text "On 1997-07-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 500m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: MU BAKER WINDOWMASTER WHIPSTOCK + MILLING ASSEMBLY & ASSOCIATED BHA. CONTINUE TIH WITH DP." "On 1997-07-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2211m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: CONTINUED TIH WITH WINDOWMASTER WHIPSTOCK & MILLING ASSEMBLY. TAGGED 9 5/8' BRIDGE-PLUG AT 2211 M DPM." "On 1997-07-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2211m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: ORIENTED WHIPSTOCK USING MWD. SET ANCHOR ON WHIPSTOCK." "On 1997-07-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2207m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CUT WINDOW IN 9 5/8' CASING USING WHIPSTOCK. TOP OF WINDOW = 2202 M MD - BOTTOM OF WINDOW = 2207 M MD. PUMPED 5 M3 HI-VIS PILL WHILE MILLING AT 2205 M." "On 1997-07-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2213m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: DRILLED/MILLED NEW FORMATION FROM 2207 - 2213 M. PUMPED 5 M3 HI-VIS PILL WHILE DRILLING AT 2208 M." "On 1997-07-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2213m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: REAMED WINDOW. AFTER APPROXIMATELY 20 TIMES, STILL UNABLE TO GO DOWN THROUGH WINDOW WITHOUT ROTATING - BASED ON USING MAXIMUM OF 12 MT WEIGHT. REAMED 5 ADDITIONAL TIMES - NOW ABLE TO SLACK-OFF & PICK-UP THROUGH WINDOW WITHOUT HAVING TO ROTATE STRING." "On 1997-07-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2196m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: PUMPED 10 M3 HI-VIS PILL & CIRCULATED HOLE CLEAN AT 2000 LPM." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2196m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: COMPLETED CIRCULATING HOLE CLEAN. FLUSHED CHOKE & KILL LINES." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1110m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: FLOW CHECKED, PUMPED SLUG & POOH TO PU DRILLING BHA." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1110m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: BURST HYDRAULIC HOSE ON UPPER RACKING ARM - REPAIRED SAME." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED TO POOH WITH MILLING ASSEMBLY." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: COMPLETED LD MILLING ASSEMBLY." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 173m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: MU DRILLING BHA; MOTOR TESTED OK." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: TIH WITH BHA TO 800 M." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 800m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: ATTEMPTED TO PERFORM WEEKLY BOP FUNCTION TEST USING YELLOW POD. NO FUNCTION OF EITHER ANNULAR POSSIBLE." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2193m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: CONTINUED TO TIH TO 2193 M WHILE PULLING YELLOW POD." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2193m. The activity was categorized as 'interruption -- maintain' and lasted for 4.0 hours. Operational details: FOUND CRIMPED PILOT LINE IN POD HOSE. CHANGED PILOT LINE FOR ANNULARS' REGULATOR. RERAN YELLOW POD & LATCHED-UP." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2193m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: FUNCTION TESTED BOPS USING YELLOW POD - FROM RIG FLOOR PANEL." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2213m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: ORIENTED BIT/MOTOR & SLACKED-OFF THROUGH WINDOW.REAMED F/2208-2212M. STARTED DRILLING-SPP INCREASED 35BAR&TDS STALLED Ø16300NM.FREED STUCK STRING USING 32 MT O/PULL-TORQUE STILL TRAPPED IN STRING.WHILE PULLING PAST 2207M W/BIT,SPP INCREASED AGAIN.FREED BIT PAST 2207M USING 55 MT O/PULL.THEN ABLE TO RELEASE TORQUE IN STRING ONCE ABOVE 2202M." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2202m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: ATTEMPTED SEVERAL TIMES TO PASS THROUGH WINDOW - UNABLE TO GO BELOW 2202 M - TOP OF WINDOW IN 9 5/8' CASING." "On 1997-07-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: FLOW CHECKED, PUMPED SLUG & POOH WITH DRILLING BHA. BIT WAS DAMAGED - 6 OUT OF 9 BLADES ON BIT WERE DAMAGED/BROKEN. NO OTHER DAMAGE TO BHA COMPONENTS NOTED." "On 1997-07-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2202m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: MU MILLING BHA & TIH TO WHIPSTOCK." "On 1997-07-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2205m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: MILLED FROM 2202-2205 M. DECREASE IN ROP - NOT MAKING ANY PROGRESS IN MILLING THROUGH WINDOW." "On 1997-07-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: FLOWCHECKED, PUMPED SLUG & POOH WITH MILLING BHA." "On 1997-07-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2187m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: TIH TO 2187 M WITH 9 5/8' BRIDGE PLUG ON DP." "On 1997-07-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2187m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: SET BRIDGE PLUG AT 2187 M L.A.T. CONFIRMED SETTING BY SLACKING-OFF 10 MT DOWN ON PLUG." "On 1997-07-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2187m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: PUMPED 10 M3 HI-VIS PILL & CIRCULATED OUT." "On 1997-07-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: FLOWCHECKED, PUMPED SLUG & POOH WITH EZSV M.S.T." "On 1997-07-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: MU BAKER WINDOWMASTER WHIPSTOCK ASSEMBLY. TIH WITH BHA ON DP." "On 1997-07-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2170m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: COMPLETED TIH WITH WHIPSTOCK TO 2170 M." "On 1997-07-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2170m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: ATTEMPTED TO CIRCULATE; STRING PLUGGED. RU & REVERSE CIRCULATED 1 DRILLSTRING VOLUME & UNPLUGGED STRING." "On 1997-07-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2187m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: ORIENTED WHIPSTOCK USING MWD. SET ANCHOR ON WHIPSTOCK." "On 1997-07-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2183m. The activity was categorized as 'interruption -- sidetrack' and lasted for 8.5 hours. Operational details: CUT WINDOW IN 9 5/8' CASING USING WHIPSTOCK. TOP OF WINDOW = 2178 M; BOTTOM OF WINDOW = 2183 M. FLOW RATE = APPROX. 1000 LPM AT 74 BAR." "On 1997-07-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2198m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: DRILLED/MILLED NEW FORMATION FROM 2183 - 2198M. FLOW RATE = 1500 LPM AT 125 BAR." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2202m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: FINISHED DRILLING TO 2202 M - TOTAL OF 19 M OF FORMATION DRILLED BEYOND WINDOW'S BOTTOM. PU & SO THROUGH WINDOW 5 TIMES - NO PROBLEMS." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2175m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: PU ABOVE TOP OF WINDOW & PUMPED 5 M3 HI-VIS PILL. CIRCULATED HOLE CLEAN AT 2000 LPM AT 195 BAR. FLUSHED CHOKE & KILL LINES & BOOSTED RISER." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: POOH TO MU DRILLING BHA." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: FINISHED HANDLING WHIPSTOCK/MILLING BHA." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 430m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: MU DRILLING BHA & TIH TO 430 M WITH NEW 8 1/2' PDC BIT." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 430m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: S/C DRILLINE." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 430m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: ELECTRICAL PROBLEM WITH TOP DRIVE SYSTEM; REPAIRED SAME." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2161m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: CONTINUED TO TIH TO 2161 M." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2161m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: ORIENTED TOOL-FACE." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2190m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH SLOWLY-NO ROTATION OR CIRCULATION-FROM 2161 - 2190 M. WINDOW IN CASING FROM 2178 - 2183 M. MADE CHECK TRIP TO 2175 M; NO PROBLEMS PASSING THROUGH WINDOW." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2202m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: BROKE CIRCULATION. WASHED DOWN FROM 2190 - 2202 M / TD." "On 1997-07-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2311m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/ORIENTED 8 1/2' HOLE FROM 2202 - 2311 M." "On 1997-07-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2405m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/ORIENTED 8 1/2' HOLE FROM 2311 - 2405 M." "On 1997-07-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2653m. The activity was categorized as 'drilling -- drill' and lasted for 13.0 hours. Operational details: DRILLED/ORIENTED 8 1/2' HOLE FROM 2405-2653 M." "On 1997-07-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2653m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED TO CLEAN HOLE." "On 1997-07-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2711m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: DRILLED/ORIENTED 8 1/2' HOLE FROM 2653 - 2711 M." "On 1997-07-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/ORIENTED 8 1/2' HOLE FROM 2711 - 2768 M. HAD PROBLEMS TURNING WELLPATH TO THE RIGHT." "On 1997-07-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED HOLE CLEAN IN PREPARATION FOR TRIP OUT." "On 1997-07-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 8.5 hours. Operational details: POOH FOR BHA CHANGE DUE TO DIRECTIONAL PROBLEM - NOT ENOUGH TURN TO RIGHT IN AZIMUTH. NOTE-NO PROBLEM IN TOH THROUGH 9 5/8' CASING WINDOW. UNABLE TO DOWNLOAD MEMORY FROM MWD AFTER TRYING FOR 1 HOUR." "On 1997-07-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: INCREASED AKO MOTOR FROM 1,2 DEGREES TO 1,5 DEGREES & MU INSERT BIT FOR DIRECTIONAL REASON/CONTROL. TIH TO 2768 M -TD. NOTE-TOOK 5 MT WEIGHT TO PASS THROUGH WINDOW WITH MOTOR/BIT." "On 1997-07-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE CLEAN IN PREPARATION FOR RUNNING GYRO SURVEY INSIDE OF DRILLSTRING. (CIRCULATION RATE = 2500 LPM AT 290 BAR.) NOTE: PREPARED/RU TO RUN GYRO WHILE CIRCULATING." "On 1997-07-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: CONTINUED CIRCULATING WHILE RU TO RUN GYRO." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: CONTINUED CIRCULATING WHILE RU TO RUN GYRO." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- survey' and lasted for 5.0 hours. Operational details: MU SIDE-ENTRY SUB INTO DRILLSTRING & RIH WITH GYRO ON ATLAS E/LINE. BIT 1 JOINT OFF BOTTOM DURING SURVEY. RAN GYRO FROM 1880 TO 2710 M. POOH WITH GYRO & RD SIDE-ENTRY SUB." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2771m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED FROM 2768 - 2771 M / SLIDING." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: DRILLED FROM 2771-2783 M. DECREASE IN ROP - TOOK APPROX. 2,5 HRS. TO DRILL LAST METER." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2190m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: FLOW CHECKED & PUMPED SLUG. POOH TO 2190 M WITH NO PROBLEMS." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2190m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: CIRCULATED W/2500LPM & ORIENTED TOOLFACE PRIOR TO PULLING THROUGH CSG. WINDOW. HOLE PACKED-OFF & STRING TORQUED-UP & LOST CIRC-STRING STUCK 2 MIN. WORKED STRING FREE BY GOING DOWNWARDS;MAX WEIGHT SLACKED-OFF=40 MT. ESTABLISHED CIRCULATION AT 600 LPM." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2199m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: WORKED STRING DOWN TO 2199 M BIT DEPTH - 16 M BELOW WINDOW'S BOTTOM. HOLE PACKED-OFF;LOST CIRCULATION SEVERAL TIMES. ATTEMPTED TO ESTABLISH CIRCULATION - IN STEPS - AT DIFFERENT FLOW RATES WHILE ROTATING AT 80- 120 RPM / PROBLEMS =PACKING-OFF,LOST CIRCULATION, TORQUING-UP OF DRILLSTRING. TORQUE WOULD INCREASE & THEN RETURNS WOULD BE LOST." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2167m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: FINALLY ESTABLISHED CIRCULATION WITH FULL RETURNS AT 1860 LPM/164 BAR. STARTED MOVING UPWARDS TOWARD WINDOW-STOPPED AT 2188 M. ORIENTED TOOL- FACE & THEN FLOW CHECKED. STARTED PULLING UP WHILE PUMPING AT 450 LPM- LOSING CIRCULATION AGAIN. STOPPED PUMPING & CONTINUED POOH-PULLED THROUGH WINDOW WITH NO ROTATING/PUMPING WITH MAXIMUM DRAG = 5 MT." "On 1997-08-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 540m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: AT 2167 M - FLOW CHECKED FOR 15 MINUTES; HOLE STATIC. FLUSHED CHOKE & KILL LINES & BOOSTED RISER CLEAN. CONTINUED TO POOH WITH BHA." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: COMPLETED POOH.INSERT BIT WAS CORED-OUT." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.5 hours. Operational details: RAN BOP TEST TOOL TO WELLHEAD.TESTED PIPE RAMS & FAIL SAFE VALVES TO 20/345 BAR; TESTED BOTH ANNULARS TO 20/241 BAR. TESTED ON YELLOW POD. FUNCTION TESTED ON BLUE POD - FROM SUBSEA CONTROL ROOM." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: COMPLETED POOH WITH BOP TEST TOOL." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 752m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: MU SLICK BHA FOR CHECK TRIP & TIH TO 752 M." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 752m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: TESTED 2-TDS SAFETY VALVES & 1-KELLY COCK TO 35/345 BAR -5/10 MINUTES." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2081m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: CONTINUED TO TIH TO 2081 M." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2183m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: ESTABLISHED CIRC AT 2500 LPM.WASHED DOWN TO CASING WINDOW. RAN THROUGH WINDOW & PU THROUGH WINDOW WITHOUT PUMPING - NO PROBLEMS. CIRCULATED AT 1500 LPM & ROTATED AT 50 RPM & RAN THROUGH WINDOW - NO PROBLEM." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2207m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: CONTINUED TIH; TOOK WEIGHT AT 2207 M. REAMED FROM 2207 - 2245 M; TIGHT HOLE FROM 2207 - 2226 M. HAD TENDENCY OF PACKING-OFF. 16300 NM= MAXIMUM TORQUE EXPERIENCED." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED TIH; WASHED DOWN LAST 38 M TO TD - 2783 M. 0,5 M OF FILL ON BOTTOM." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED AT 2500 LPM - 204 BAR - TO CLEAN HOLE. WORKED BIT ON BOTTOM BECAUSE OF PREVIOUS BIT'S CONDITION. EXCESSIVE AMOUNT OF CUTTINGS BACK DURING CIRCULATION; AFTER BOTTOMS UP, CAVINGS STARTED TO RETURN TO SURFACE." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: INCREASED MUD WEIGHT FROM 1,50 SG TO 1,54 SG WHILE CIRCULATING AT 2200 LPM. AFTER 1,54 MUD AROUND, INCREASED FLOW RATE TO 2500 LPM - 210 BAR - WITH NO LOSSES." "On 1997-08-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2231m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: FLOW CHECKED, PUMPED SLUG & POOH TO MU DRILLING BHA." "On 1997-08-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2231m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: WITH TOP OF DCS 10M BELOW WINDOW, CIRCULATED BOTTOMS UP AT 2231 M BIT DEPTH. 2000 LPM = 127 BAR. NO UNUSUAL AMOUNT OF CUTTINGS AT SHAKERS." "On 1997-08-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONTINUED POOH - MAXIMUM DRAG THROUGH WINDOW = 2,25 MT." "On 1997-08-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: MU NEW INSERT BIT - EHP43AFLDK - & MU SLICK DRILLING BHA WITH MOTOR & MWD." "On 1997-08-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: RIH TO 2160M. ESTABLISHED CIRC WITH 2500 LPM AND ORIENTED TOOLFACE. RUN THROUGH WINDOW WITH NO ROTATION OR CIRCULATION AND CONTINUED RIH WITH NO PROBLEMS. WASHED LAST STAND TO TD." "On 1997-08-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2970m. The activity was categorized as 'drilling -- drill' and lasted for 13.0 hours. Operational details: DRILLED AND ORIENTED 8 1/2' HOLE FROM 2783 - 2970 M." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3052m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED AND ORIENTED 8 1/2' HOLE FROM 2970 M - 3052 M." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3057m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3052 - 3057 M / ROTATING." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3057m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: CIRCULATED HOLE CLEAN & BOOSTED RISER. HAD EXCESSIVE AMOUNT OF CUTTINGS OVER THE SHAKERS." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2707m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: MADE SHORT TRIP TO 2707 M & RIH TO TD - WASHED DOWN LAST STAND TO TD - NO PROBLEMS." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3057m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CIRCULATED HOLE CLEAN & BOOSTED RISER. SHORT TRIP GAS=4,38% CORRECTED." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2253m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH TO 2253 FOR BIT & BHA CHANGE." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2253m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: WITH TOP OF DCS 10 M BELOW CASING WINDOW, CIRCULATED BOTTOMS UP AT 2000 LPM. ORIENTED TOOLFACE AT 55 DEGREES & PULLED THROUGH WINDOW WITH NO OVERPULL." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: COMPLETED POOH." "On 1997-08-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1270m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: MU NEW PDC BIT WITH STABILIZED DRILLING BHA; PU NEW MOTOR DUE TO WEAR. TIH TO 1270 M." "On 1997-08-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2135m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED TO TIH TO 2135 M." "On 1997-08-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2210m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: FILLED DRILLSTRING. CIRCULATED AT 1985 LPM /196 BAR ; ORIENTED BIT TO 65 DEG. RIGHT & RIH THROUGH CASING WINDOW." "On 1997-08-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3057m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: COMPLETED TIH TO TD-3057 M. WASHED LAST STAND TO BOTTOM - NO FILL." "On 1997-08-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3057m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: TOOK SCRS. INCREASE IN GAS TO 6,9 % - CORRECTED. COMPLETED CIRCULATING BOTTOMS UP PRIOR TO DRILLING. GAS DECREASED TO 0,5 %. STARTED DRILLING 8 1/2' HOLE AT 0546 HRS." "On 1997-08-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3369m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3057 - 3369 M." "On 1997-08-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3379m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3369 - 3379 M. HAD INCREASING AMOUNT OF CAVINGS IN RETURNS." "On 1997-08-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3379m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED UNTIL SHAKERS CLEANED-UP BECAUSE OF INCREASE IN HOLE DRAG. BOOSTED RISER & FLUSHED CHOKE/KILL LINES. FLOW RATE = 2500 LPM. NOTE: EXCESSIVE AMOUNT OF CUTTINGS TO SURFACE; TOOK 3 BOTTOMS UP FOR SHAKERS TO CLEAN-UP." "On 1997-08-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3390m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3379 - 3390 M." "On 1997-08-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3494m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: DRILLED 8 1/2'' HOLE FROM 3390 - 3494 M." "On 1997-08-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3494m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED UNTIL SHAKERS CLEANED UP BECAUSE OF INCREASE IN TORQUE + DRAG AND INCREASE OF PRESENCE OF CASINGS. BOOSTED RISER." "On 1997-08-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3550m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED 8 1/2'' HOLE FROM 3494 - 3550 M." "On 1997-08-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3552m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED 8 1/2'' HOLE FROM 3550 - 3552 M." "On 1997-08-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3552m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED UNTIL SHAKERS CLEANED UP BECAUSE OF INCREASE IN DRAG + IN PREPARATION TO ORIENT. BOOSTED RISER. NOTE: EXCESSIVE AMOUNT OF LARGE CASINGS TO SURFACE; TOOK 2.5 X BOTTOMS UP FOR SHAKERS TO CLEAN UP." "On 1997-08-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3573m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: DRILLED 8 1/2'' HOLE FROM 3552 - 3573 M. UNABLE TO STEER DUE TO HANGING UP ON STABILIZERS AND FREQUENT STALLING PROBLEMS." "On 1997-08-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- drill' and lasted for 9.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3573M TO 3632M. UNABLE TO STEER TO ACHIVE TARGET." "On 1997-08-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: CIRC HOLE CLEAN. DROP CARBIDE, EST HOLE SIZE 10,47 IN. CAVINGS RATE AT 100 L/HR AFTER CIRC 1,5 BTM UP. BOOSTED RISER." "On 1997-08-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.5 hours. Operational details: FLOW CHECK 10 MIN, OK. PUMP SLUG. POOH. WELL SLICK. FLOW CHECK INSIDE SHOE AND BEFORE BHA ENTERED BOP. L/DOWN 1 DC, 2 STABILIZERS AND BIT." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1040m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: MADE UP NEW BIT, SET AKO TO 1,5 DEGR TILT, UNLOAD MWD AND M/UP NEW JAR AND RIH TO 1040M." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1040m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: FILL DRILL PIPE AND TEST MWD. FAIL TO GET SIGNALS FROM MWD. RE-BOOT MWD COMPUTER AND GOT SIGNALS OK." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2160m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUE RIH TO 2160M." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2160m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: SLIP AND CUT DRILLING LINE." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2160m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: CONTINUED TO SLIP AND CUT 33,5M DRILLING LINE." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2185m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: ORIENTED TOOL FACE AND ENTERCSG WINDOW. P/UP 4-5 T DRAG OUTSIDE WINDOW" "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: RIH TO 3612M. WASHED DOWN TO BTM AT 3632M." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3653m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: DRILL 8 1/2' HOLE IN ORIENTED MODE FROM 3632 TO 3653M. NO SIGNALS FROM MWD." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2653m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: CIRC UNTIL SHAKERS CLEARED UP. BOOSTED RISER." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2700m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: FLOW CHECK, OK. PUMP SLUG. POOH TO CHANGE MWD." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2700m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: ATTEMPT TO GET COMMUNICATION WITH MWD WITHOUT SUCCESS." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1220m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: PUMP SLUG. POOH. GOT 15 T DRAG AT 1220M." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1220m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CIRC 1,25 BTM UP AT 1220M. BOOST RISER. GOT FAIR AMOUNT OF LARGE SIZE TYPE CAVINGS OVER SHAKERS." "On 1997-08-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: FLOW CHECK, OK CONTINUE POOH AND L/DOWN MWD AND BIT. START RELOAD NEW MWD." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CONTINUE CHANGE MWD AND LOAD SAME. M/UP NEW BIT." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2160m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: RIH TO CSG WINDOW AT 2160M. TESTED MWD OK AT 1000M." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2185m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: FILL PIPE AND ORIENTED TOOL FACE AND ENTER INTO CSG WINDOW WITHOUT OBSTRUCTIONS." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3056m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: CONTINUED RIH TO CURRENT DEPTH 3085M." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3653m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: CONTINUED RIH TO 3640M. WASH TO BTM AT 3653M. NO FILL." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3673m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3653 - 3673M. FLOW CHECK DRILLING BREAK AT FROM 3670M - 3673M." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3673m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRC FOR GEOLOGHICAL SAMPLES." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3724m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: CONTINUED DRILLING FROM 3673M - 3724M. FLOW CHECK AT 3717M." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3724m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRC FOR GEOLOGHICAL SAMPLES." "On 1997-08-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3752m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: CONTINUED DRILLING FROM 3724M - 3752M." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3783m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING F/3752 - 3783M. USED CONSTANT PARAMETERS TO SPOT DRILLING BREAK." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3799m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3783M - 3799M. DRILLING BREAK 3796 - 3799M." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3799m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 1.5 hours. Operational details: CIRC FOR GEOLOGICAL SAMPLES. BOOSTED RISER." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3810m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: CONTINUED DRILLING FROM 3799M - 3810M." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3810m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 1.5 hours. Operational details: CIRC FOR GEOLOGICAL SAMPLES. BOOSTED RISER." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: CONTINUED DRILLING FROM 3810M - 3820M." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 0.5 hours. Operational details: CIRC FOR GEOLGICAL SAMPLE." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3823m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: CONTINUED DRILLING FROM 3820M - 3823M." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3823m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRC HOLE CLEAN. BOOSTED RISER." "On 1997-08-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 978m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: FLOW CHECK, OK. PUMP SLUG AND POOH. HOLE IN GOOD CONDITION." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUED POOH TO SURFACE." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CHANGED BIT. SET AKO TO 0,6 DEGR. FUNCTION TEST SHEAR RAM FROM YELLOW POD." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: DUMP MEMORY ON MWD." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH TO GET BHA BELOW BOP." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: TEST BOP FUNCTIONS FROM YELLOW POD. ALL OK." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2004m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED RIH TO CURRENT DEPTH 2004M. FILL PIPE, TESTED MWD AT 1000M ." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3823m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONTINUED RIH. BREAK CIRC AND WASH LAST STAND TO BTM. CIRC TO CLEAR STEEL DEBRIS OFF BTM." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3837m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3823M - 3837M. MWD INDICATE SAND AT 3822M" "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3837m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 2.0 hours. Operational details: CIRC FOR GEOLOGICAL SAMPLES." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.5 hours. Operational details: FLOW CHECK, OK. PUMP SLUG. POOH. FLOW CHECKED AT 2163M AND WITH BHA BELOW BOP." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: LAYED OUT BIT AND DOWNLOADED MWD." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: MADE UP 27M COREBARREL AND PDC CORHEAD." "On 1997-08-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 100m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: STARTED TO RIH WITH CORING BHA." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3212m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.5 hours. Operational details: CONT RIH WITH CORING BHA. FILL PIPE AT CSG WINDOW. RIH PASS WINDOW AND PULL BACK INTO CSG WITH COREBARREL, OK. CONT RIH TO 3212M. WORK AWAY 15T OBSTRUCTION AT 3008M AND 3174M. DID NOT GET CORRECT AMOUNT OF MUD IN RETURNS." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3212m. The activity was categorized as 'formation evaluation -- core' and lasted for 0.5 hours. Operational details: BREAK CIRC AND FILLED PIPE TOO EARLY. FLOAT VALVE NOT OPERATING CORRECT. CIRC 1 STRING CONTENT AND GOT 6.6% GASPEAK FROM 65M. FLOW CHECK, OK." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3303m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: CONTINUE RIH. STOOD UP WITH 15T AT 3287M. REAMED OBSTRUCTION. CONT RIH AND STODD UP AT 3303M. CURRENTLY REAMING AWAY OBSTRUCTION." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- trip' and lasted for 10.5 hours. Operational details: WASH AND REAM TIGHT HOLE FROM 3303 - 3820M WITH COREBARREL BHA." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BTMS UP AT 3820M." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3837m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: CONTINUED WASH AND REAM TIGHT HOLE FROM 3820M - 3837M." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3837m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: TAG BTM AND SPACED OUT. DROP BALL AND SEATED SAME WITH 14 BAR OVER PRESSURE. TAKE SCR'S." "On 1997-08-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3849m. The activity was categorized as 'formation evaluation -- core' and lasted for 3.5 hours. Operational details: START CORING FROM 3837-3849M. STALLED OUT ON BTM TWICE DURING FIRST 2M CORING. PULLED OFF BTM AND RE-STARTED." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3854m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.5 hours. Operational details: CONTINUED CUT CORE FROM 3849 - 3854M. CORE JAMMED, TORQUE DROPPED OFF AND PRESSURE DEGREASED. ATTEMPT TO RESTART CORING, NOT ABLE TO OBTAIN TORQUE ON BTM." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1244m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.5 hours. Operational details: FLOW CHECK, OK. PUMP SLUG AND POOH. HAD 15T OVER PULL AT 3278 AND 3269M. FLOW CHECKED INSIDE CSG WINDOW, OK. CONT POH. CURRENT DEPTH AT REPORT TIME, 1244M." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: CONTINUED POOH TO SURFACE. PULLED LAST 400M WITH RESTRICTED SPEED, 6 MIN/STAND. FLOW CHECKED BEFORE PULLED BHA." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: RETRIEVED CORE NO 1, 95 % RECOVERY." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.5 hours. Operational details: BREAK CH AND CHANGED ALL STABS FROM 8 15/16' TO 8 3/8' ON CORE BARREL MADE UP CORE HEAD." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2161m. The activity was categorized as 'formation evaluation -- trip' and lasted for 5.0 hours. Operational details: RIH TO CSG WINDOW AT 2161M. FILL STRING EACH 1000M." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2161m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: SLIP AND CUT 29,3M DRILLING LINE." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3830m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.0 hours. Operational details: CONTINUED RIH TO 3830M. BREAK CIRC." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3854m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: REAM TO BTM 3854M. 2M HARD FILL. TAG BTM 3 TIMES AND SPACED OUT STRING" "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3854m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: DROP BALL AND SEATED SAME IN COREBARREL WITH 17 BAR PRESS INCREASE. TAKE SCR'S." "On 1997-08-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3858m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.0 hours. Operational details: START CUT CORE NO 2 FROM 3854 - 3858M." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3881m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.5 hours. Operational details: CONTINUED CORING FROM 3858 - 3881M. TOTAL CUT 27M." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3852m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: FLOW CHECKED, OK. LAID DOWN SPACER PUP JT. PUMP SLUG." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 780m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.0 hours. Operational details: POOH. FLOW CHECKED INSIDE CSG WINDOW, OK. CURRENT DEPTH AT REPORT TIME, 780M." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.0 hours. Operational details: CONTINUED POOH WITH CORE NO 2. REDUCED SPEED LAST 400M. HELD SAFETY BRIEF BEFORE PULL CORE BARREL TO DRILL FLOOR. HAD 20 PPM H2S IN COREBARREL. PERSONNEL PUT ON PROTECTION EQUIPMENT BEFORE START LAYING DOWN CORE." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: RETRIVED CORE NO 2, 100 % RECOVERY. MAX 5 PPM H2S WHEN RETRIVING CORE." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: M/UP COREBARREL AND COREHEAD. SERVICED COREBARREL." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2160m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.0 hours. Operational details: RIH TO CSG WINDOW AT 2161M. BREAK CIRC EACH 1000 M." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2160m. The activity was categorized as 'formation evaluation -- wait' and lasted for 0.5 hours. Operational details: HELD SAFETY MEETING WITH ALL PERSONNEL WITH H2S GAS, GAS PROCEDYRES AND CONTINGENCIES." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3876m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: CONTINUED RIH TO 3876M." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3876m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRC BTM'S UP IN ORDER TO CLEAN WELL FOR GAS. MAX PEAK FROM PREVIOUS CORING; 15,2 %. CIRC GAS LEVEL DOWN TO 0,9 %." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3881m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: ROTATE AND WASH TO BTM AT 3881,5M. SPACED OUT STRING." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3881m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: DROP BALL AND SEATED SAME IN COREBARREL WITH 17 BAR PRESS INCREASE. TAKE SCR'S." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3908m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.5 hours. Operational details: CUT CORE NO 3 FROM 3881,5 TO 3908,5M." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: PUMP OUT OF HOLE TO 3820M. HAD 45 T OVER PULL AT CONNECTION AT 3880M. ROTATE STRING AND HAD NO EXCESSIVE TORQUE TO BREAK ROTATION, NORMAL PUMP PRESSURES INDICATING GEOMETRICAL OBSTRUCTION." "On 1997-08-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRC TO CLEAN OUT CORING GAS." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: CONTINUED CIRC BTM'S UP. MAX GAS FROM CORING 12,75 % DECLINED TO 2,8 %" "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1412m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.0 hours. Operational details: FLOW CHECKED OK. PUMP SLUG AND POOH. FLOW CHECKED INSIDE CSG WINDOW.OK CURRENT DEPTH AT REPORT TIME 1412M." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: CONTINUED POOH WITH CORE NO 3. FLOW CHECKED AT CSG WINDOW AND BEFORE PULLING BHA INTO BOP." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: RETRIEVED CORE NO 3. INITIAL TOP OF CORE HAD 80 PPM H2S GAS CONTENT WHICH DISPERSED, CHECKS WHILE RETRIEVING WERE 10 PPM DOWN TO 0 PPM. 99,6 % CORE RECOVERY." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: SERVICED CORE BARREL AND MADE UP COREBARREL WITH INNERBARREL." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- trip' and lasted for 6.0 hours. Operational details: RIH TO 3820M. BROKE CIRC EACH 1000M." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3908m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: WASH AND ROTATE FROM 3820 TO BTM AT 3908,5M." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3908m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRC BTM'S UP IN ORDER TO CLEAN WELL FOR GAS. MAX GAS 4,5 %, DECLINED TO 1 %." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3908m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.0 hours. Operational details: DROP BALL AND SPACE OUT STRING. SEATED BALL IN COREBARREL WITH 17 BAR PRESSURE INCREASE. TAKE SCR'S." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3935m. The activity was categorized as 'formation evaluation -- core' and lasted for 2.0 hours. Operational details: CUT CORE NO 4 FROM 3908,5 TO 3935,5M. MAX GAS FROM CORING 9%." "On 1997-08-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: BROKE CORE ON 3RD ATTEMPT HOLDING 16T OVER PULL. PUMPED AND ROTATED SLOWLY WHILE PULLING BACK TO 3820M." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED BTM UP TO CLEAN WELL FOR CORING GAS. MAX GAS 0,7 %" "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1195m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.0 hours. Operational details: FLOW CHECKED, OK. PUMP SLUG AND POOH. FLOW CHECKED INSIDE CSG WINDOW, OK. CURRENT DEPTH AT REPORT TIME 1195M." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.0 hours. Operational details: CONTINUED TO POOH. FLOW CHECKED BEFORE PULLING BHA INTO BOP, OK." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: RETRIEVED CORE NO 4. 96,3 % RECOVERY. NO H2S GAS PRESENT IN COREBARREL" "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: MADE UP NEW COREHEAD AND INNERBARREL. SERVICED COREBARREL." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3847m. The activity was categorized as 'formation evaluation -- trip' and lasted for 6.0 hours. Operational details: RIH WITH COREBARREL TO 3847M. BROKE CIRCULATION EACH 1000M." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3935m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: WASHED AND ROTATED FROM 3847M TO 3935,5M." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3935m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.0 hours. Operational details: TAGGED BTM AND SPACED OUT. SEATED BALL IN BALL SEAT WITH 26 BAR PRESSURE INCREASED. RECORDED SCR'S." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3962m. The activity was categorized as 'formation evaluation -- core' and lasted for 2.0 hours. Operational details: CUT CORE NO 5 FROM 3935,5M TO 3962,5M. BROKE CORE WITH 11 TON OVER PULL." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: PUMPED AND ROTATED UP TO 3820M." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BTM UP TO CLEAN WELL FROM CORING GAS. MAX GAS 2,1 % DECLINED TO 0,8 %." "On 1997-08-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3600m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: FLOW CHECKED, OK. PUMPED SLUG AND POOH TO 3600M AT 2400 HRS." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 25m. The activity was categorized as 'formation evaluation -- trip' and lasted for 6.0 hours. Operational details: CONTINUED POOH. FLOW CHECKED AT CSG WINDOW AND BEFORE BHA ENTERED BOP. CHECKED COREBARREL FOR H2S GAS, NO GAS PRESENT." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: RECOVERED CORE NO 5. 102 % RECOVERY. NO H2S GAS DETECTED FROM COREBARREL." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: MADE UP COREHEAD AND INNERBARREL, SERVICED COREBARREL." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3905m. The activity was categorized as 'formation evaluation -- trip' and lasted for 5.0 hours. Operational details: RIH WITH COREBARREL TO 3905M. BROKE CIRCULATION EACH 1000M." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3962m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: WASHED AND ROTATED FROM 3905M TO 3962M." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3962m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: TAGGED BTM AT 3962,5M AND SPACED OUT. SEATED BALL IN BALL SEAT WITH 29 BAR PRESSURE INCREASE. RECORDED SCR'S" "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3990m. The activity was categorized as 'formation evaluation -- core' and lasted for 2.5 hours. Operational details: CUTTED CORE NO 6 FROM 3962,5M TO 3990M. BROKE CORE WITH 10 T OVER PULL." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: PUMPED AND ROTATED UP TO 3820M." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED BTM UP TO CLEAN WELL FROM CORING GAS. MAX GAS 1,7 % DECLINED TO 0,8 %." "On 1997-08-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1400m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.5 hours. Operational details: FLOW CHECKED , OK. PUMPED SLUG AND POOH TO 1400M AT 2400 HRS. HAD FLICKERS ON WEIGHT INDICATOR AT 2725 AND 2472M, MAX 22 T OVER PULL FLOW CHECKED IN CSG WINDOW, OK." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: CONTINUED POOH. FLOW CHECKED, OK, BEFORE BHA ENTERED BOP. HELD RESTRICTED SPEED FROM 400M AND TO SURFACE." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: RECOVERED CORE NO 6. 100.5 % RECOVERY." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 26m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: MADE UP NEW COREHEAD AND INNERBARREL, SERVICED COREBARREL." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 600m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: RIH WITH COREBARREL TO 600M." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2162m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: CONTINUED RIH TO CSG WINDOW. BROKE CIRCULATION." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2162m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: SLIP AND CUT 36,6 M DRILLING LINE." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3924m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: CONTINUED RIH TO 3924M." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3990m. The activity was categorized as 'formation evaluation -- trip' and lasted for 8.5 hours. Operational details: PUMPED AND ROTATED FROM 3924M TO 3933M. REAMED TIGHT SPOT AT 3933M TO 3936M. FREQUENTLY STALLED STRING AND HAD MAX 90T OVERPULL. CONTINUED REAMING TO BTM AT 3990M WITH STALLING CONDITIONS." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3990m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.0 hours. Operational details: TAGGED BTM AT 3990M AND SPACED OUT. SEATED BALL IN BALL SEAT WITH 18 BAR PRESSURE INCREASE. RECORDED SCR'S." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4017m. The activity was categorized as 'formation evaluation -- core' and lasted for 3.0 hours. Operational details: CUTTED CORE NO 7 FROM 3990M TO 4017M. BROKE CORE WITH NO SIGNIFICANT OVERPULL." "On 1997-08-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3990m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: PUMPED AND ROTATED UP TO 3990M." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: CONTINUED PUMPING AND ROTATION UP TO 3820M." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.5 hours. Operational details: CIRCULATED BTM UP TO CLEAN WELL FROM CORING GAS. MAX GAS 2,9 % DECLINED TO 0,15 %. FLOW CHECKED, OK." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2546m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: PUMPED SLUG. POOH WITH CORE NO 7. CURRENT DEPTH AT REPORT TIME 2546 M." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.5 hours. Operational details: CONTINUED POOH WITH CORE NO 7. FLOW CHECKED IN CSG WINDOW AND BEFORE BHA ENTERED BOP, OK." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: RECOVERED CORE NO 7. 98,9 % RECOVERY. NO H2S GAS PRESENT IN COREBARREL" "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- core' and lasted for 2.0 hours. Operational details: SERVICE BREAK AND LAID DOWN COREBARREL." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: MADE UP BOP TEST PLUG AND INSTALLED SAME IN WELLHEAD." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: TESTED BOP AND PLUG TO 34 BAR/5 MIN AND 345 BAR/10 MIN. USED YELLOW POD." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: ATTEMPTED TO TEST UIBOP, VALVE LEAKED. RIGGED DOWN TEST LINE." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: CONTINUED TEST BOP FROM YELLOW POD. TESTED ALL VALVES AND PIPE RAMS TO 34/345 BAR FOR 5/10 MIN. TESTED BOTH ANNULARS TO 34/241 BARS. FUNCTION TESTED WITH BLUE POD FROM TP REMOTE PANEL. ALL WHILST REPAIR ON UIBOP." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RETRIVED TEST PLUG. LAID DOWN STABILIZER STAB AND TEST PLUG." "On 1997-08-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: CHANGED OUT UIBOP ON TDS. RENEWED SAVER SUB AND NEW PIPEHANDLER HANGER UIBOP ACTUATOR, CRANK LEVER, ACTUATOR ROLLERS." "On 1997-08-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CONTINUED TO ASSEMBLE AND ADJUST LEVER FOR UIBOP ACTUATOR." "On 1997-08-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: CONTINUED TEST ON UIBOP AND LIBOP TO 34/345 BAR 5/10 MIN, OK." "On 1997-08-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CHANGED MWD. SET NAVIDRILL AKO TO 0 DEGR. LOAD MWD AND MADE UP BIT." "On 1997-08-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 630m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: RIH TO CURRENT DEPTH 630M." "On 1997-08-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3824m. The activity was categorized as 'drilling -- trip' and lasted for 7.0 hours. Operational details: CONTINUED RIH WITH DRILLING BHA TO 3824M. BROKE CIRCULATION EACH 1000M PERFORMED CHECK SHOTS WITH NEW MWD AT 3794M AND 3805M, OK." "On 1997-08-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4017m. The activity was categorized as 'formation evaluation -- log' and lasted for 8.5 hours. Operational details: WASHED AND ROTATED WHILST LOGGING CORED INTERVAL WITH MWD FROM 3805M TO 4003M." "On 1997-08-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4039m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 4017M TO 4039M." "On 1997-08-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING FROM 4039M TO 4087M. NORMAL AMOUNT OF CUTTINGS IN RETURNS WITH APPROX 5% SMALL SIZE CAVINGS." "On 1997-08-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4131m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 4087M TO 4131M." "On 1997-08-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4131m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 4.0 hours. Operational details: CIRCULATED AND CONDITIONED HOLE AND MUD FOR LOGGING." "On 1997-08-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 8.5 hours. Operational details: FLOWCHECKED, PUMPED SLUG, AND POOH. DUMPED MWD MEMORY. L/D MWD AND MOTOR." "On 1997-08-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: R/U ATLAS WIRELINE." "On 1997-08-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: FINISHED R/U ATLAS. RIH WITH FIRST LOG RUN: HDIL-MAC-DGR-CHT. LOGGING TOOL STOOD UP AT 2755M. ATTEMPTED TO WORK PAST W/O SUCCESS - TOOL STOOD UP AT SAME PLACE AND PICKED UP CLEANLY EACH TIME. LOGGED OUT FROM 2755M." "On 1997-08-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: FINISHED LOGGING RUN #1: HDIL-MAC-DGR-CHT. R/D LOGGING TOOLS." "On 1997-08-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 9.0 hours. Operational details: R/U TO RUN TO RUN VSP ON WIRELINE AND RIH. TOOL STOOD UP AT 2762M. LOGGED OUT OF HOLE WITH VSP." "On 1997-08-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: R/U TO RUN LOGS ON DRILL PIPE." "On 1997-08-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: REPAIRED TOP DRIVE - BOLTS SHEARED ON SWIVEL LINK PINION CLAMP (PART OF TDS/TRAVELLING BLOCK RETRACT SYSTEM)." "On 1997-08-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: FINISHED REPAIRING TOP DRIVE." "On 1997-08-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 227m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: FINISHED R/U AND BEGAN RIH WITH LOGS ON DRILL PIPE. HDIL-MAC-ZDL-CND-SPL-CHT-VSP" "On 1997-08-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3610m. The activity was categorized as 'formation evaluation -- log' and lasted for 18.0 hours. Operational details: CONTINUED RIH WITH LOGGING TOOLS ON DRILL PIPE: HDIL-MAC-ZDL-CND-SPL- CHT-VSP. EXPERIENCED PROBLEMS WITH A DISCONTINUOUS SIGNAL AT +\- 2825M - 2840M." "On 1997-08-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4120m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.5 hours. Operational details: CONTINUED RUNNING LOGS ON DRILL PIPE. PROBLEM WITH DISCONTINUOUS SIGNAL FROM +\- 3845M - 3872M, 4018M - 4024M, 4045M - 4120M." "On 1997-08-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4040m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: BEGAN LOGGING OUT OF THE HOLE WITH VSP." "On 1997-08-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2730m. The activity was categorized as 'formation evaluation -- log' and lasted for 9.0 hours. Operational details: CONTINUED LOGGING OUT OF THE HOLE WITH VSP ON DRILL PIPE." "On 1997-08-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4125m. The activity was categorized as 'formation evaluation -- log' and lasted for 8.0 hours. Operational details: RIH WITH LOGGING TOOLS ON DRILL PIPE." "On 1997-08-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4090m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: LOGGED OUT OF HOLE ON DRILL PIPE: HDIL-MAC-ZDL-CND-SPL-CHT." "On 1997-08-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3513m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.0 hours. Operational details: CONTINUED LOGGING OUT OF HOLE ON DRILL PIPE: HDIL-MAC-ZDL-CND-SPL-CNT. SOME PROBLEMS WITH BAD/DISCONTINUOUS SIGNAL IN THE BEGINNING BUT IT WAS CORRECTED AND A GOOD LOG IS BEING ACQUIRED." "On 1997-08-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2144m. The activity was categorized as 'formation evaluation -- log' and lasted for 5.5 hours. Operational details: CONTINUED LOGGING OUT OF HOLE ON DRILL PIPE: HDIL-MAC-ZDL-CND-SPL-CHT." "On 1997-08-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2144m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: POOH WITH WET CONNECTOR (WIRELINE). BROKE AND LAID OUT SIDE ENTRY SUB AND WET CONNECTOR." "On 1997-08-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.0 hours. Operational details: POOH WITH LOGGING TOOLS ON DRILL PIPE. MEANWHILE AWS CHANGED OUT WIRELINE DRUM." "On 1997-08-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: BROKE AND LAID OUT LOGGING TOOLS." "On 1997-08-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: AWS THREADED WIRELINE THROUGH SIDE ENTRY SUB AND RE-HEADED WIRE." "On 1997-08-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: AWS RE-TERMINATED AND CHECKED OUT WIRELINE DRUM COLLECTOR." "On 1997-08-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: CHECKED TOOLS FOR NEXT LOGGING RUN: FMT-ZDL-MAC-HDIP-CHT. BEGAN R/U TO RIH ON DRILL PIPE." "On 1997-08-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: R/U LOGGING TOOLS TO RUN ON DRILL PIPE: FMT-ZDL-MAC-HDIP-CHT." "On 1997-08-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 9.5 hours. Operational details: POOR SIGNAL FROM LOGGING TOOLS. DISMANTLED AND RE-TERMINATED WIRELINE DRUM COLLECTOR. CUT 700 METERS OF WIRE. RE-HEADED WIRE TO THROUGH SIDE ENTRY SUB TO WET CONNECTOR. RE-CHECKED TOOL STRING." "On 1997-08-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 263m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: BEGAN RIH WITH LOGGING TOOLS ON DRILL PIPE." "On 1997-08-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 263m. The activity was categorized as 'formation evaluation -- wait' and lasted for 4.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO INDUSTRIAL ACTION." "On 1997-08-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 352m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: RESUMED RIH WITH LOGGING TOOLS ON DRILL PIPE." "On 1997-08-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1677m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.0 hours. Operational details: CONTINUED RIH WITH LOGGING TOOLS ON DRILL PIPE TO CASING WINDOW." "On 1997-08-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2168m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: CONTINUED RIH WITH LOGGING TOOLS ON DRILL PIPE TO 2168M (BOTTOM OF LOGGING TOOL STRING)." "On 1997-08-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2168m. The activity was categorized as 'formation evaluation -- wait' and lasted for 16.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO INDUSTRIAL ACTION. MEANWHILE CIRCULATED AT SLOW RATE - 330 LPM, 15 BAR." "On 1997-08-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2168m. The activity was categorized as 'formation evaluation -- wait' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO INDUSTRIAL ACTION. CONTINUED CIRCULATING AT 330 LPM, 15 BAR." "On 1997-08-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2168m. The activity was categorized as 'formation evaluation -- wait' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO INDUSTRIAL ACTION. CIRCULATED AT 330 LPM, 15 BAR." "On 1997-08-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2168m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: R/U WIRELINE SIDE ENTRY SUB AND RIH WITH WET CONNECTOR. ENGAGED CONNECTOR. COMMUNICATION AND PULL TESTED OK." "On 1997-08-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3640m. The activity was categorized as 'formation evaluation -- log' and lasted for 7.0 hours. Operational details: RIH WITH LOGGING TOOLS ON DRILL PIPE TO 3640M." "On 1997-08-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3640m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: CIRCULATED TO CONDITION MUD." "On 1997-08-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4123m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: CONTINUED RIH WITH LOGGING TOOLS ON DRILL PIPE. LOST SIGNAL TO LOGGING TOOLS AT 3800M." "On 1997-08-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4123m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: PIPE STUCK WHILE MAKING UP TOP DRIVE. WORKED PIPE WITH NO SUCCESS. ATLAS SHEARED CLAMP ON SIDE ENTRY SUB AND POOH WITH WIRELINE IN ORDER TO GAIN ROTATION OF DRILL PIPE." "On 1997-08-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4123m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: ATLAS POOH WITH WET CONNECTOR TO SIDE ENTRY SUB AND SHEARED OUT OF ROPE SOCKET WITH 5.4 MT PULL. ATLAS FINISHED POOH WITH WIRELINE. WORKED PIPE FREE WITH ROTATION AND RECIPROCATION." "On 1997-08-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3530m. The activity was categorized as 'formation evaluation -- log' and lasted for 7.0 hours. Operational details: BACKREAMED FROM 4123M TO 3530M. MAXIMUM OVERPULL 32 MT." "On 1997-08-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.0 hours. Operational details: PUMPED SLUG, FLOWCHECKED, AND POOH." "On 1997-08-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: ATLAS BROKE DOWN AND L/D LOGGING TOOL STRING." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: ATLAS CONTINUED BREAK OUT AND L/D LOGGING TOOL STRING." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1921m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: M/U BIT AND BHA AND RIH FOR WIPER TRIP TO CONDITION HOLE FOR RUNNING 7' CASING." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2158m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CONTINUED RIH FOR WIPER TRIP TO CONDITION HOLE AND MUD FOR RUNNING 7' CASING." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2158m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: CUT AND SLIPPED DRILLING LINE." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4047m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: FINISHED RIH." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4047m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CIRCULATED." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3800m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: BACKREAMED FROM 4047M TO 3800M." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3800m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: CIRCULATED TO CONDITION MUD FOR RUNNING 7' CASING - LOWERED AND EVENED MUD WEIGHT TO 1.55 SG FROM HIGH SPOTS OF 1.58 SG TO 1.61 SG." "On 1997-08-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 421m. The activity was categorized as 'drilling -- casing' and lasted for 6.5 hours. Operational details: POOH TO RUN 7' CASING." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: FINISHED POOH. L/D DRILLING JAR." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: P/U SL TOOL (WEAR BUSHING RETRIEVING TOOL), RIH, AND RETRIEVE WEAR BUSHING (NO DISCERNIBLE WEAR OR MARKS)." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: M/U CASING HANGER WITH SEAL ASSEMBLY TO TYPE ST CASING HANGER RUNNING TOOL C/W SSR PLUGS. M/U HALLIBURTON CEMENTING HEAD." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: R/U FRANK'S FC-1 CASING FILLUP AND CIRCULATING TOOL. R/U WEATHERFORD CASING EQUIPMENT." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: FINISHED R/U WEATHERFORD TO RUN 7' CASING." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1030m. The activity was categorized as 'drilling -- casing' and lasted for 9.5 hours. Operational details: RAN 7' CASING." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1030m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: HYDRAULIC POWER UNIT FOR CASING TONG OVERHEATED." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1669m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RAN 7' CASING." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1699m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CASING TONG NOT WORKING - PROBLEM WITH HYDRAULIC PRESSURE/VOLUME SUPPLY. CHANGED POWER UNITS." "On 1997-08-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1837m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RAN 7' CASING." "On 1997-09-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2539m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONTINUED RUNNING 7' CASING." "On 1997-09-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3935m. The activity was categorized as 'drilling -- casing' and lasted for 13.0 hours. Operational details: CONTINUED RUNNING 7' CASING." "On 1997-09-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3935m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: M/U CASING HANGER. R/D CASING HANDLING TOOLS AND R/U TO RUN CASING ON DRILL PIPE." "On 1997-09-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4044m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH WITH CASING ON HWDP RUNNING STRING. LANDED CASING AND CHECKED DATUM LINE - OK. TOTAL MUD LOSSES RUNNING CASING - 6 M3." "On 1997-09-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4044m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: CIRCULATED CASING. 20% - 30% MUD RETURNS WHILE CIRCULATING AT 330 LPM - 475 LPM. LOST 26 M3 MUD TOTAL." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4044m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PUMPED 15 M3 HALLIBURTON SPACER 50OE+. GAINED 2 M3 (13 M3 LOST). DROPPED BALL AND SHEARED OUT BOTTOM PLUG WITH 100 BAR." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4044m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: BATCHED UP AND MIXED AND PUMPED 10.1 M3 1.80 SG CEMENT. DROPPED DART AND SHEARED TOP PLUG WITH 230 BAR." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4044m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: DISPLACED CEMENT. PUMP RATE 475 LPM, 10% MUD RETURNS. LOST 68 M3 MUD WHILE DISPLACING CEMENT. CIRCULATING PRESSURE FROM TIME BOTTOM PLUG HIT FLOAT COLLAR (CEMENT BEHIND BOTTOM PLUG) UNTIL TOP PLUG BUMPED ROSE 13 BAR (12 BAR CALCULATED). BUMPED PLUG WITH 70 BAR OVER FCP TO 132 BAR. FLOATS HELD OK." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4044m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: SET SEAL ASSEMBLY. PRESSURE TEST FAILED - RETURNS COMING UP DRILL STRING. BEGIN POOH." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: TEST OF SEAL ASSEMBLY FAILED. POOH WITH ST CASING HANGER RUNNING TOOL." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: FOUND SEALS ON ST TOOLS TO BE WASHED OUT. ATTEMPTED TO TEST SEAL ASSEMBLY AGAINST BLIND RAMS WITHOUT SUCCESS." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: M/U SEAL ASSEMBLY RUNNING TOOL AND RIH. RE-TORQUED SEAL ASSEMBLY AND ATTEMPTED TO PRESSURE TEST WITHOUT SUCCESS." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: M/U SL TOOL. RIH AND RETRIEVED SEAL ASSEMBLY." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: M/U MILL/FLUSH TOOL AND RIH. MILLED AND FLUSHED SEAL AREA AT TOP OF CASING HANGER - WELLHEAD. PUMPED 5 M3 HIVIS AND BOOSTED RISER. POOH." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: M/U SEAL ASSEMBLY RUNNING TOOL WITH ELASTOMER TYPE SEAL ASSEMBLY AND RIH. SET SEAL ASSEMBLY AND TESTED TO 345 BAR OK. POOH." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.5 hours. Operational details: M/U SL TOOL AND 7' WEAR BUSHING AND RIH. SET WEAR BUSHING IN WELLHEAD AND TESTED BOP TO 35/345 BAR ON YELLOW POD FROM MAIN PANEL. FUNCTION TESTED ON BLUE POD FROM TOOLPUSHERS MINIPANEL. FUNCTION TESTED ACOUSTIC CONTROLS FROM CELLAR DECK. POOH." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: FOUND WEAR BUSHING NOT RELEASED FROM SL TOOL. RIH AND RE-SET WEAR BUSHING. POOH." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: R/D CEMENTING HEAD AND L/D SAME." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: CHANGED XO SUB ON BOTTOM OF EMERGENCY HANGOFF TOOL FOR 3 1/2' DRILL PIPE." "On 1997-09-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: R/U TO RUN 3 1/2' DRILL PIPE. START RIH WITH SAME." "On 1997-09-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1337m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: CONTINUED P/U AND RIH WITH 3 1/2' DRILL PIPE." "On 1997-09-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2530m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: COMPLETED PU & RIH WITH 3 1/2' DP TO 2530 M." "On 1997-09-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2636m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: TIH TO WELLHEAD WITH HANG-OFF-TOOL.SECURED WELL WITH MIDDLE 5' PIPE RAMS. BACK-OUT OF H-O-T. POOH WITH LANDING STRING." "On 1997-09-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: CLOSED BLIND SHEAR RAMS. TESTED 7' CASING TO 345 BAR." "On 1997-09-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: DISPLACED RISER TO SEAWATER. RU SPIDER & MU DIVERTER RUNNING TOOL." "On 1997-09-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 9.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE." "On 1997-09-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE." "On 1997-09-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-09-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-10-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATIONS SUSPENDED DUE TO OFS STRIKE." "On 1997-10-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE." "On 1997-10-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE." "On 1997-10-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE" "On 1997-10-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE" "On 1997-10-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE" "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE" "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 11.0 hours. Operational details: OPERATION SUSPENDED DUE TO OFS STRIKE." "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: LAID OUT DIVERTER RUNNING TOOL AND SPIDER." "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 102m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH WITH OPEN ENDED 5' DP TO TOP OF SHEARRAM." "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 102m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: DISPLACED RISER AND KILL AND CHOKELINES TO OBM. VERIFIED NO PRESSURE UNDER BOP." "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2620m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: OPENED SHEARRAM. SCREWED INTO HANG-OFF TOOL. PULLED HANG-OFF TOOL OVER BOP." "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2636m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: BROKE CIRCULATION AND CIRCULATED BOTTOMS UP." "On 1997-10-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2575m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: SLUGGED PIPE AND POOH TO 2575 M." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: CONTINUED POOH WITH 3 1/2' DP TO 170 M." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH FROM 170 M WITH 3 1/2' DP." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: RIH WITH 4 STDS OF 3 1/2' DP BELOW BOP TEST TOOL. OD ON XO SUB BELOW TEST TOOL WAS TOO BIG TO ENTER 7' CSG. TEST PLUG WAS NOT SEATED. POOH AND RACKED BACK 3 1/2' DP." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: UNSCREWED EXTENSION SUB FROM BOP TEST TOOL. PU 9JTS X 5' HWDP FROM DECK. RIH AND SEATED BOP TEST TOOL." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.5 hours. Operational details: TESTED BOP ON BLUE POD. TESTED ALL VALVES AND RAMS TO 20/345 BAR. TESTED ANNULAR TO 20/241 BAR. FUNCTION TESTED BOP ON YELLOW POD." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: POOH WITH TEST TOOL. FUNCTION TESTED ACCUSTIC SYSTEM AND SHEARRAM." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: TESTED IBOPS ON TOPDRIVE AND STAB-IN VALVES TO 20/345 BAR." "On 1997-10-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 5.0 hours. Operational details: LD 70 JTS OF 5' DP FROM DERRICK." "On 1997-10-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 6.0 hours. Operational details: CONTINUED LD 5' DP. LAID DOWN TOTAL 144 JTS." "On 1997-10-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: LD 5' DP FROM DERRICK." "On 1997-10-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 226m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 3.5 hours. Operational details: CHANGED HANDLING TOOLS AND MU 5 7/8' BIT AND 7' CSG SCRAPER. PU 9 JTS OF 4 3/4' DC AND 15 JTS OF 3 1/2' HWDP FROM DECK AND RIH." "On 1997-10-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1502m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 4.5 hours. Operational details: RIH TO 1502 M WITH 3 1/2' DP FROM DERRICK. BROKE CIRCULATION AT 1000 M." "On 1997-10-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1502m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 3.5 hours. Operational details: LD 15 JTS OF 5' HWDP AND 9 JTS OF 6 1/2' DC FROM DERRICK." "On 1997-10-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2550m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 6.0 hours. Operational details: PU 3 1/2'DP FROM DECK. RIH TO 2550 M. BROKE CIRCULATION AT 2000 M AND 2500 M." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2718m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.0 hours. Operational details: CONTINUED PU 3 1/2' DP FROM DECK. RIH TO 2718 M." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 4.5 hours. Operational details: RIH WITH STANDS TO 3820 M. BROKE CIRCULATION AT 3000 M AND 3500 M." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: INSTALLED XO SUB AND 5' PUP JOINT. CONNECTED TOP DRIVE AND WORKED CSG SCRAPER OVER PACKER SETTING AREA FROM 3795 M TO 3820 M. PUMPED 850 LPM - 310 BAR SPP." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3820m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: WORKED CASING SCRAPER OVER PACKER SETTING AREA FROM 3795 M TO 3820 M. CIRCULATED 850 LPM - 310 BAR STAND PIPE PRESSURE." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3850m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH TO 3850 M. HAD BACKFLOW THROUGH DRILLSTRING DUE TO UNBALANCED MUD." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3850m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED AND CONDITION MUD AT 3850 M." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3950m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH TO 3950 M. HAD BACKFLOW THROUGH DRILLSTRING." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3950m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED AND CONDITION MUD AT 3950 M." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4019m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: WASHED DOWN FROM 3950 M. TAGGED FLOAT COLLAR AT 4019 M." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4019m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.5 hours. Operational details: CIRCULATED AND CONDITION MUD TO 1.55 SG." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 9.0 hours. Operational details: SLUGGED PIPE AND POOH. LD 5 7/8' BIT AND 7' CSG SCRAPER." "On 1997-10-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: HELD PRE-JOB MEETING WITH ALL PERSONNEL INVOLVED. RU TO RUN SHOOTING NIPPLE ON 7' CASING. PU XO SUB FOR WIRELINE STUFFING BOX AND MU TO JOINT OF 7' CASING. LD SAME ON DECK." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 92m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: PU SHOOTING NIPPLE AND RIH WITH SAME ON 7' CASING TO 92 M." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 92m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: INSTALLED XO SUB FOR WIRELINE SHIEVE ON TOP DRIVE SAVER SUB. CHANGED TO 45 FT BAILS." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: WESTERN / ATLAS MADE UP SBT - CCL - GR." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: WESTERN / ATLAS INVESTIGATED POWER FAILURE ON LOGGING TOOL. CHANGED OUT SWIVEL AND MU NEW CONNECTION." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: PU CASING JOINT WITH XO SUB AND STUFFING BOX. CONNECTED LOGGING CABLE." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: WESTERN / ATLAS HAD INDICATION OF PERIODICAL FAILURE ON LOGGING TOOL. CHANGED OUT CABLE HEAD." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 65m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH WITH SBT-CCL-GR TO 65 M. MU LAST CASING JOINT. POSITIONED STRING WITH HEAVE COMPENSATOR AND CLOSED LOWER ANNULAR." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1440m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: WESTERN/ATLAS RIH WITH SBT-CCL-GR. TOOL STOOD UP AT 1270 M. WORKED TOOL DOWN. STOOD UP AGAIN AT 1440 M. TRIED TO WORK THROUGH; NO SUCCESS." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: POOH WITH WIRELINE. DISCONNECTED UPPER CASING JOINT AND LD LOGGING TOOL." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: INSTALLED WTS TOOLS BELOW SBT TO ALLOW FOR MORE WEIGHT." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 150m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: TOOL CHECK SHOWED FAILURE ON VDL SECTION. CHANGED TO BACK UP TOOL. PERFORMED NEW TOOLCHECK. OK. RIH TO 150 M AND INSTALLED UPPER CASING JOINT." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4019m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: RIH WITH SBT-CCL-GR. CHECKED PICK UP WEIGHT AT 1000 M / 2500 LBS - 2000 M / 3600 LBS - 2500 M / 5600 LBS. AT 3000 M PICK UP WEIGHT (PUW) WAS 8000 LBS, LOGGING WEIGHT (LW) WAS 7500 LBS. AT 3500 M WE SHOWED PUW / LW = 8000 / 7500 LBS. AT TD ( 4036 M WIRELINE DEPTH ) WE SHOWED PUW / LW = 10000 / 9500 LBS." "On 1997-10-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3556m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: LOGGED FROM 3993 M TO 3556 M." "On 1997-10-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2592m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: LOGGED FROM 3556 M TO 2592 M." "On 1997-10-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH FROM 2592 M WITH LOGGING TOOL." "On 1997-10-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: LD UPPER CASING JOINT. LD LOGGING TOOL AND RIGGED DOWN WIRELINE." "On 1997-10-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: CHANGED BAILS AND LD HANG-OFF SUB FOR LOGGING SHIEVE." "On 1997-10-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: L/D 7' LINER / SHOOTING NIPPLE EQUIPMENT. BROKE AND L/D STUFFING BOX EQUIP." "On 1997-10-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: PREPARED FOR RUNNING ATLAS MAC LOG. R/D ATLAS WIRELINE." "On 1997-10-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4019m. The activity was categorized as 'drilling -- trip' and lasted for 14.0 hours. Operational details: M/U AND RIH W/ 5-7/8' BIT AND 7' CSG SCRAPER FOR MUD CONDTION/ CLENAUP RUN. BROKE CIRC. EVERY 500 M. CIRC. TO CONDITION MUD. RECORDED TORQUE/ DRAG EACH 500 M. RIH TO FC (4019 M). TREATED MUD. MW DRIFTED BACK FROM 1,55 SG TO 1,47 SG." "On 1997-10-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4019m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: CIRCULATED TO CONDITION MUD, 820 LPM / 300 BAR. HAD PROBLEMS W/ UNSTABLE MW. CIRC. UNTIL EVEN 1,47 SG." "On 1997-10-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH FROM 4019 M TO 3200 M." "On 1997-10-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1630m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH W/ 5-7/8' BIT FROM 3200 M TO 1630 M." "On 1997-10-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1630m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: FLUSHED KILL-/CHOKE LINES. CIRC. TO CONDITION MUD (1300 LPM)." "On 1997-10-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: POOH W/ 5-7/8' BIT FROM 1630 M. RACKED BHA IN DERRICK." "On 1997-10-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: R/U ATLAS WIRELINE. M/U MAC TOOL STRING." "On 1997-10-10, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3500m. The activity was categorized as 'workover -- wire line' and lasted for 9.5 hours. Operational details: RAN ATLAS LOG NO. 2 B: MAC-GR. IH: 1430 HRS. OOH: 2344 HRS." "On 1997-10-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: R/D ATLAS LOG NO. 2B: MAC-GR." "On 1997-10-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: M/U ATLAS PERFORATING GUN ASSY." "On 1997-10-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3550m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: RIH W/ ATLAS PERFORATING GUN ASSY. IH: 0235 HRS. RECORDED PICK-UP WT AS RIH; 2000 M: 3000 LBS, 2500 M: 4000 LBS, 3000 M: 5300 LBS, 3500 M: 6600 LBS." "On 1997-10-11, at Well NO 15/9-19 A, a drilling event occurred at a depth of 4016m. The activity was categorized as 'workover -- wire line' and lasted for 18.0 hours. Operational details: RAN ATLAS PERFORATING GUN ON WIRELINE. FIRED 2 FIRST LEVELS. NO INDIC. OF FIRING. POOH. OOH: 1420 HRS. VERIFIED BOTH LEVELS FIRED. RIH: 1435 HRS. FIRED REMAINING 5 LEVELS; HAD INDIC. OF FIRING FIRST 2 LEVELS. POOH." "On 1997-10-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: CONT. POOH W/ ATLAS PERF. RUN ASSY. OOH: 0020 HRS. FOUND 3 UPPER UPPER LEVELS NOT FIRED, AND LOWEST 2,6 M OF GUN ASSY. LEFT IN HOLE." "On 1997-10-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: SLIPPED / CUT DRILLING LINE WHILE TROUBLE SHOOTING ON ATLAS EQUIP." "On 1997-10-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: WORKED ON ATLAS LOGGING EQUIPMENT." "On 1997-10-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: M/U AND RIH W/ ATLAS PERFORATING GUN. IH: 0450 HRS." "On 1997-10-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3963m. The activity was categorized as 'interruption -- other' and lasted for 16.0 hours. Operational details: RIH W/ ATLAS PERF. GUN ASSY. NOT ABLE TO PASS 3505 M. POOH. ADDED WEIGHTS. RIH. FIRED LEVEL 5 AND 6 INSIDE 7' CSG. SKIPPED LEVEL 7, DUE TO NOT ABLE TO CORRELATE. POOH. OOH 2145 HRS. R/D LOGGING TOOLS." "On 1997-10-12, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: P/U AND M/U SCHLUMBERGER MDT TOOL STRING." "On 1997-10-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: M/U SCHLUMB. MDT TOOL STRING." "On 1997-10-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: CONNECTED CABLE TO SCHLUMB. MDT TOOL STRING. TESTED SIGNALS. GOT INDIC. OF CONTACT FAILURE IN TOOL STRING." "On 1997-10-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: WORKED TO SOLVE CONTACT FAILURE IN SCHLUMB. MDT TOOL STRING." "On 1997-10-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: WORKED TO SOLVE CONTACT FAILURE IN SCHLUMB. MDT TOOL STRING. FOUND CONTACT FAILURE ON CHAMBRE MODULE. REPAIRED SAME. TESTED MDT ASSY." "On 1997-10-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3602m. The activity was categorized as 'workover -- wire line' and lasted for 14.5 hours. Operational details: M/U SCHLUMB. MDT TOOL STRING TO 3-1/2' DP AND RIH, SPEED: 2 MIN/STD. FILLED PIPE EVERY 3. STD, BROKE CIRC. EVETY 10. STD. RIH TO 3602 M." "On 1997-10-13, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3602m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: LAUNCHED LOCOMOTIVE INTO DP, INSTALLED SIDE ENTRY SUB. RAN/PUMPED LOCOMOTIVE INSIDE 3-1/2' DP ON ATLAS CABLE." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3602m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: CONT. RUNNING/PUMPING LOCOMOTIVE INTO DP ON ATLAS CABLE. LATCHED SAME ONTO MDT TOOL STRING." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3602m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: TESTED CABLE CONNECTION TO SCHLUMB. MDT TOOL STRING." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3602m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: HAD CONTACT FAILURE W/ PACKER MODULE ON SCHLUMB. MDT TOOL STRING. WORKED TO SOLVE PROBLEM. UNLATCHED/LATCHED LOCOMOTIVE; MAX. 9500 LBS TENSION ON CABLE. NOT ABLE TO GET PROPER SIGNALS W/ PACKER MODULE ON MDT TOOL STRING. POOH W/ CABLE." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: POOH W/ ATLAS CABLE. CHECKED SINGNALS AT SURFACE; CABLE OK." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.5 hours. Operational details: POOH W/ SCHLUMB. MDT TOOL ASSY. FROM 3602 M." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: WORKED TO LOCATE PROBLEM IN SCHLUMB. MDT TOOL ASSY. LOCATED FAULT IN FLUID ANALYZER. CHANGED OUT SAME. TESTED OUT TOOL STRING." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 860m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: M/U AND RIH W/ SCHLUMB. MDT TOOL ASSY. ON 3-1/2' DP; SPEED: 2 MIN/STD. FILLED PIPE EVERY 3. STD, BROKE CIRC. EVERY 10 STD. RIH TO 860 M." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 860m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: REPAIRED ON BROKEN HYDRAULIC HOSE ON UPPER RACKING ARM." "On 1997-10-14, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1800m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: CONT. RIH W/SCHLUMB. MDT TOOL ASSY. ON 3-1/2' DP FROM 860 M TO 1800 M." "On 1997-10-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3600m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: CONT. RIH W/SCHLUMB. MDT TOOL ASSY. ON 3-1/2' DP FROM 1800 M TO 3600 M." "On 1997-10-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3600m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: LAUNCHED LOCOMOTIVE INTO DP, INSTALLED SIDE-ENTRY SUB. RAN/PUMPED LOCOMOTIVE INSIDE 3-/2' DP ON ATLAS CABLE." "On 1997-10-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3600m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: PUMPED LOCOMOTIVE DOWN DP ON ATLAS CABLE. LATCHED SAME ONTO MDT TOOL STRING. ATTEMPTED TO GET GOOD TEST SIGNALS FROM MDT; NEG. UNLATCHED / LATCHED LOCOMOTIVE. NO IMPROVMENT. POOH W/ ATLAS CABLE. CHECKED CABLE SIGNALS AT SURFACE; OK." "On 1997-10-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 7.0 hours. Operational details: POOH W/SCHLUMB. MDT TOOL ASSY. FROM 3600 M. L/D MDT ASSY." "On 1997-10-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: P/U AND M/U MODIFIED MDT TOOL ASSY.; REDUCED ASSY. W/ 3 MODULES. TESTED SIGNALS; OK." "On 1997-10-15, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1960m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: RIH W/SCHLUMB. MDT TOOL ASSY. ON 3-1/2' DP TO 1960 M. SPEED: 2 MIN/STD FIRST 500 M, THEN 1 MIN/STD. FILLED PIPE EVERY 3. STD, BROKE CIRC. EVERY 10. STD." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3604m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: CONT. RIH W/SCHLUMB. MDT TOOL ASSY. ON 3-/2' DP FROM 1960 M TO 3604 M." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3604m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: LAUNCHED LOCOMOTIVE INSIDE 3-1/2' DP, INSTALLED SIDE-ENTRY SUB. RAN/PUMPED LOCOMOTIVE INSIDE DP ON ATLAS CABLE. LATCHED SAME ONTO MDT TOOL ASSY." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3604m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: TESTED SCHLUMB. MDT SIGNALS THROUGH ATLAS CABLE. GOOD TEST." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3604m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: FINISHED TESTING MDT." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3604m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: CHAMBER VALVE ON MDT NOT OPERATING. ATTEMPTED TO TROUBLESHOOT AND REPAIR WITHOUT SUCCESS." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3604m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: PULLED LOCOMOTIVE TO SURFACE. CHECKED OUT CABLE - OK." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3360m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: PUMPED SLUG AND POOH TO 3360M." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3360m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 8.0 hours. Operational details: CIRCULATED AND CONDITONED MUD." "On 1997-10-16, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: SLUGGED PIPE AND POOH WITH MDT TOOL." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: L/D MDT TOOL." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3955m. The activity was categorized as 'workover -- perforate' and lasted for 4.5 hours. Operational details: R/U ATLAS AND RIH WITH ATLAS PERFORATING GUNS ON WIRELINE. CORRELATED GUN DEPTH AND FIRED GUNS - GOOD INDICATION OF DETONATION. ATLAS POOH." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: POOH WITH ATLAS WIRELINE PERFORATING GUNS." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.0 hours. Operational details: RIH WITH BOP TEST TOOL. TESTED BOP TO 20/345 BAR (UAP TO 20/240 BAR) FOR 5/10 MINUTES ON YELLOW POD. FUNCTIONED TESTED BOP ON BLUE POD." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: M/U LUBRICATOR #1 TO SINGLE 5' TUBING AND L/D SAME." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: TESTED TDS IBOP'S TO 20/345 BAR FOR 5/10 MINUTES." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 5.0 hours. Operational details: M/U LUBRICATOR #2 TO SINGLE 5' TUBING AND L/D SAME. M/U FLUTED HANGER AND L/D SAME. M/U FLOWHEAD AND L/D SAME." "On 1997-10-17, at Well NO 15/9-19 A, a drilling event occurred at a depth of 185m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.0 hours. Operational details: P/U DST BHA INCLUDING 19 X 4-3/4' DRILL COLLARS." "On 1997-10-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 238m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: CONTINUED P/U DST BHA + 1 STAND 3-1/2' DP." "On 1997-10-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 238m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: FILLED TEST STRING WITH 1500 L HIVIS MUD AND DIESEL. PRESSURE TESTED TO 345 BAR." "On 1997-10-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 238m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: FINISHED PRESSURE TESTING DST STRING TO 345 BAR." "On 1997-10-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3828m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 14.5 hours. Operational details: RIH W/ 3-1/2' DP TEST STRING FILLING WITH DIESEL AS CUSHION." "On 1997-10-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3829m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: TESTED DST STRING TO 345 BAR." "On 1997-10-18, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: M/U FLUTED HANGER AND MADE DUMMY RUN ON 5' DP. LANDED IN WELLHEAD AND OPERATED MPR'S. POOH AND L/D FLUTED HANGER." "On 1997-10-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3828m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: CLEANED AND CLEARED RIG FLOOR. P/U UMBILICAL REEL AND CONTROL PANEL. MADE UP FLUTED HANGER AND SSTT. FUNCTIONED SSTT." "On 1997-10-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: RIH WITH TEST STRING ON 5' TUBING. P/U AND FUNCTIONED 2 X SUBSEA LUBRICATOR VALVES." "On 1997-10-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CONTINUED RIH WITH TEST STRING." "On 1997-10-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: TESTED DST STRING AGAINST TESTER VALVE TO 345 BAR. INFLOW TESTED SSTT WITH 345 BAR. INFLOW TESTED LUBRICATOR VALVES WITH 345 BAR. TESTED LOWER LUBRICATOR VALVE TO 345 BAR." "On 1997-10-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 10.0 hours. Operational details: INSTALLED 45'BAILS. INSTALLED WIRELINE BOP ON FLOWHEAD. INSTALLED KILL AND FLOWLINE COFLEX HOSES TO FLOWHEAD. P/U AND M/U FLOWHEAD. INSTALLED KILL AND FLOWLINE COFLEX HOSES TO STANDPIPES. HOOK UP CONTROL HOSES TO FLOWHEAD AND WIRELINE BOP." "On 1997-10-19, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 4.5 hours. Operational details: LANDED FLUTED HANGER IN WELLHEAD. TESTED KILL COFLEX LINE TO 345 BAR. TESTED DST STRING AGAINST TESTER VALVE TO 345 BAR. INFLOW TESTED MASTER VALVE WITH 345 BAR. INFLOW TESTED KILL WING VALVE WITH 345 BAR. FLUSHED ACROSS FLOWHEAD AND THROUGH FLOW WING VALVE TO BURNER HEADS." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: TESTED FLOWLINE TO CHOKE MANIFOLD TO 345 BAR." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: SET PACKER AT 3937M." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: HELD PRE-TEST SAFETY MEETING. CHECKED SURFACE VALVES LINES UP CORRECTLY. TESTED ESD SYSTEM." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 3.5 hours. Operational details: OPENED TESTER VALVE AND INITIATED MAIN FLOW PERIOD OF WATER ZONE." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.0 hours. Operational details: CONTINUED MAIN FLOW PERIOD OF WATER ZONE. POOR RESPONSE, WELL DIED BEFORE WATER REACHED SURFACE." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: SHUT IN WELL WITH SELECT TESTER VALVE TO CHECK OPERATION OF VALVE." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: OPENED WELL AND CONTINUED FLOW PERIOD. NO RESPONSE FROM WELL." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 5.5 hours. Operational details: SHUT IN WELL WITH UPPER SUBSEA LUBRICATOR VALVE. R/U WIRELINE LUBRICATOR AND MWS BOTTOM HOLE SAMPLER/GR/CCL." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'interruption -- other' and lasted for 6.5 hours. Operational details: RIH WITH MWS BOTTOM HOLE SAMPLING TOOL. SAMPLE CHAMBER FAILED TO OPEN. POOH WITH WIRELINE." "On 1997-10-20, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WAITED ON SWELL AND HEAVE TO SUBSIDE TO DISCONNECT WIRELINE LUBRICATOR AND CHANGE OUT BOTTOM HOLE SAMPLING TOOL. RIG HEAVING 2M-3M." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: CONTINUED WAITING FOR SWELL AND HEAVE TO SUBSIDE TO DISCONNECT WIRELINE LUBRICATOR AND CHANGE OUT BOTTOM HOLE SAMPLING TOOLS. RIG HEAVE 2M-3M." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: RIG HEAVE LESS THAN 2M. DISCONNECTED WIRELINE LUBRICATOR AND CHANGED OUT BOTTOM HOLE SAMPLING TOOLS." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: INSTALLED WIRELINE LUBRICATOR AND TESTED TO 345 BAR." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3200m. The activity was categorized as 'workover -- wire line' and lasted for 4.5 hours. Operational details: RIH WITH MWS BOTTOM HOLE SAMPLING TOOL/GR/CCL AND OBTAINED WATER SAMPLE. POOH." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: L/D SAMPLING TOOL/GR/CCL." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 3.5 hours. Operational details: CYCLED OMNI VALVE TO CIRCULATING POSITION. REVERSE CIRCULATED TUBING CONTENTS TO MUD AND COLLECTED FORMATION WATER SAMPLES. OBSERVED WELL. CIRCULATED TUBING TO SEAWATER. CYCLED OMNI TO TEST POSITION." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: ATTEMPTED TO PERFORM MINI-FRAC. PRESSURED TUBING TO 345 BAR, PRESSURE DROPPED TO 210 BAR IN 2 MINUTES AND THEN TO 50 BAR AFTER 3 MORE MINUTES. COULD NOT ESTABLISH INJECTION RATE." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 4.5 hours. Operational details: CYCLED OMNI VALVE TO CIRCULATING POSITION. REVERSE CIRCULATED TUBING TO MUD. CYCLED OMNI TO TEST POSTION." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: R/D WIRELINE PRESSURE CONTROL EQUIPMNENT. MEANWHILE FLOWCHECKED WELL." "On 1997-10-21, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: P/U STRING AS HIGH AS POSSIBLE TO UNSEAT PACKER." "On 1997-10-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: ATTEMPTED TO ESTABLISH INJECTION DOWN ANNULUS - PACKER SET (PACKER HAD NOT COME UNJAYED BEFORE AND RESET WHEN STRING WAS SLACKED OFF TO LAND FLUTED HANGER IN WELLHEAD)." "On 1997-10-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3930m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.5 hours. Operational details: L/D FLOWHEAD AND DISCONNECTED COFLEX LINES. CHANGED ELEVATOR BAILS." "On 1997-10-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.0 hours. Operational details: LANDED FLUTED HANGER IN WELLHEAD. OPENED RD CIRCULATING VALVE AND LOCKED OPEN SELECT TESTER VALVE." "On 1997-10-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3937m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.5 hours. Operational details: CIRCULATED BOTTOMS UP. MAXIMUM GAS 8.7%. FLOWCHECKED. PUMPED SLUG." "On 1997-10-22, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 15.5 hours. Operational details: POOH WITH DST STRING. L/D LUBRICATOR VALVES AND SUBSEA TEST TREE. CHECKED ROTARY TORQUE - MAX 9000 FT X LBS. CONTINUED POOH. L/D DST TOOLS. MEANWHILE, AFTER DST TOOLS ABOVE BOP, CLOSED BSR'S AND ATTEMPTED TO ESTABLISH INJECTION INTO PERFORATIONS - NO LEAK OFF AT 200 BAR (WITH 1.48 MUD AT 3156M TVD = 2.13 SG EMW)." "On 1997-10-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2200m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.0 hours. Operational details: P/U 7' EZSV RETAINER AND RIH TO 2200 M." "On 1997-10-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3940m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.5 hours. Operational details: COMPLETED TIH WITH 7' EZSV TO 3940 M." "On 1997-10-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3940m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: CROWN-MOUNTED-COMPENSATOR WOULDN'T UNLOCK - CMC HYDRAULIC VALVE WAS STUCK IN CLOSED POSITION. TROUBLESHOOTED SYSTEM UNTIL VALVE WAS FREED & CMC UNLOCKED." "On 1997-10-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3947m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: ATTEMPTED TO SET EZSV AT 3940 M - NO SUCCESS IN SETTING. ATTEMPTED TO SET AT 3945 M - NO SUCCESS. FINALLY SET EZSV AT 3947 M - DIDN'T SEE ANY OVERPULL TO SHEAR-OFF OF EZSV BUT SUCCESSFUL IN SETTING 22,5 MT DOWN ONTO EZSV." "On 1997-10-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3947m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: PRESSURE TESTED EZSV TO 345 BAR FOR 15 MINUTES." "On 1997-10-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3920m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 3.0 hours. Operational details: CIRCULATED 1 COMPLETE CIRCULATION WHILE S/C DRILLINE." "On 1997-10-23, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3400m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH WITH EZSV MECHANICAL SETTING TOOL." "On 1997-10-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.0 hours. Operational details: COMPLETED POOH WITH EZSV MECHANICAL SETTING TOOL. PERFORMED WEEKLY FUNCTION TEST OF BOPS WHEN SETTING TOOL LOCATEDØ480M. FUNCTION TESTED ON YELLOW POD FROM TOOLPUSHER'S OFFICE." "On 1997-10-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: PU USED SSTT & BROKE-OUT ASSOCIATED TUBULARS. LD SSTT & PU BACK-UP SSTT. MU ASSOCIATED TUBULARS & LD ON PIPE RACK FOR PRESSURE TESTING." "On 1997-10-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: PU BACK-UP FLOW HEAD & MU 1 JOINT OF 5' TBG. BELOW HEAD. LD FLOW HEAD ON PIPE RACK FOR PRESSURE TESTING." "On 1997-10-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3888m. The activity was categorized as 'workover -- perforate' and lasted for 6.0 hours. Operational details: RU ATLAS ELECTRIC LINE. RIH & PERFORATED DST #1A ZONE FORM 3885,5 - 3888,5 M AT 6 SPF. POOH & RD ATLAS." "On 1997-10-24, at Well NO 15/9-19 A, a drilling event occurred at a depth of 220m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 7.5 hours. Operational details: HELD PRE-JOB SAFETY MEETING. MU DST BHA." "On 1997-10-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 317m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: COMPLETED MU DST BHA. TESTED TO 345 BAR FOR 10 MINUTES." "On 1997-10-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 674m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: CONTINUED RUNNING DST STRING - PU/MU 3 1/2' PH-6 TUBING FOR TESTING. FILLING TUBING WITH BASE OIL EVERY 7 JOINTS. 38 JOINTS PU/MU AS OF REPORT TIME." "On 1997-10-25, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3758m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 18.0 hours. Operational details: CONTINUED RUNNING DST STRING - PU/MU 3 1/2' PH-6 TUBING FOR TESTING. FILLING TUBING WITH BASE OIL EVERY 7 JOINTS." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3758m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: COMPLETED P/U AND M/U 3 1/2' TUBING. RAN A TOTAL OF 358 JTS." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: M/U DUMMY FLUTED HGR. AND RIH ON 5' DP. LANDED IN WEAR BUSHING. CLOSED MPR TO MARK PIPE." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: R/U AWS AND MWS. RUH WITH GR/CCL AND CORRELATED DEPTH." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: POOH WITH ELECTRIC LINE AFTER CORRELATION RUN. RD ATLAS/MWS." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3758m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: CLOSED MPR FOR SPACE-OUT PURPOSES. OPENED RAMS & POOH WITH DUMMY FLUTED HANGER. LD HANGER." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3757m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: CLEANED RIG FLOOR. RAN 2 PUP JTS. 3 1/2' TBG. FOR SPACE-OUT. PRESSURE TESTED DST STRING AGAINST LPR-N VALVE TO 345 BAR FOR 10 MINUTES. PU WEIGHT = 113 MT; SO WEIGHT = 68 MT." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3758m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: PU SSTT & MU SAME INTO TEST STRING." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3758m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: SSTT WOULDN'T RE-LATCH DURING FUNCTION TEST. LD SSTT & PU BACK-UP SSTT." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3758m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: FUNCTION TESTED LATCHING MECHANISM ON SSTT." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3827m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: RIH WITH 5' LANDING STRING." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3840m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.0 hours. Operational details: MU 2 LUBRICATOR VALVES + ASSOCIATED TUBULARS TO LANDING STRING. PRESSURE TESTED DST STRING AGAINST LPR-N VALVE TO 345 BAR FOR 10 MINUTES. TESTED SSTT VALVES & LUBRICATOR VALVES AS PER TEST PROCEDURE." "On 1997-10-26, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.0 hours. Operational details: MU 1 JT. 5' TBG. MU FLOWHEAD & RU ASSOCIATED HOSES." "On 1997-10-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: COMPLETED RU FLOWHEAD." "On 1997-10-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: LANDED FLUTED HANGER INTO WEAR BUSHING. TEST FLOWHEAD, TEST STRING, & TESTING EQUIPMENT AS PER TEST PROCEDURE." "On 1997-10-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: ESTABLISHED WEIGHTS: PU = 122 MT; SO = 82 MT. SET 7' RTTS PACKER Ø 3799 M. LANDED HANGER BACK INTO WEAR BUSHING. CLOSED MPR. CHECKED THAT SURFACE VALVES CORRECTLY LINED-UP. TESTED ESD SYSTEM FROM 2 POINTS-RIG FLOOR & CHOKE MANIFOLD. HELD SAFETY BRIEFING ON RIG FLOOR." "On 1997-10-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 16.5 hours. Operational details: OPENED WELL VIA LPR-N VALVE Ø 0645 HRS. FLOWED 11 M3 BASE OIL CUSHION TO STOCK TANK - THEN SWITCHED TO FLARE BOOM. FLOWED & TESTED WELL." "On 1997-10-27, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.5 hours. Operational details: SHUT-IN WELL Ø 2233 HRS. BY CLOSING LPR-N VALVE. MONITORED SHUT-IN SURFACE PRESSURE FOR 1 HOUR TO INSURE THAT LPR-N VALVE WASN'T LEAKING." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.0 hours. Operational details: VERIFIED THAT LPR-N VALVE WASN'T LEAKING.CLOSED LOWER LUBRICATOR VALVE & PERFORMED 10 MINUTE IN-FLOW TEST. CLOSED UPPER LUBRICATOR VALVE. BLED PRESSURE OFF OF SURFACE LINES THROUGH CHOKE MANIFOLD & FLUSHED LINES TO STOCK TANK WITH SEAWATER." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.0 hours. Operational details: WHILE CONTINUING WITH SHUT-IN PRESSURE BUILD-UP TEST, RU ELECTRIC LINE IN PREPARATION FOR FUTURE WIRELINE SAMPLING." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.0 hours. Operational details: CONTINUED PERFORMING SHUT-IN BUILD-UP TEST." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 8.5 hours. Operational details: CONTINUED PERFORMING SHUT-IN BUILD-UP TEST." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: OPENED WELL & FLOWED IN PREPARATION OF BOTTOM-HOLE-SAMPLING *BHS* OPERATIONS. SHUT-IN WELL Ø 1645 HRS." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3765m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 5.0 hours. Operational details: RU 4 BHS TOOLSTRING ON ATLAS ELECTRIC LINE. TESTED LUBRICATOR/BOPS TO 200 BAR. RIH WITH BHS TO 3765 M - WELL WAS OPENED-UP AFTER TOOLSTRING WAS BELOW 500 M." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3765m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.5 hours. Operational details: SHUT-IN WELL. PERFORM BHS OPERATIONS." "On 1997-10-28, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: POOH WITH BHS / ELECTRIC LINE." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: COMPLETED POOH WITH BHS / ELECTRIC LINE." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 3.0 hours. Operational details: RD BHS TOOLSTRING. ANALYZED/CHECKED SAMPLERS FOR ACCEPTABLE SAMPLES." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: START PERFORMING MINI-FRAC BY PUMPING/BULLHEADING SEAWATER/POLYMER DOWN TEST STRING." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 3.0 hours. Operational details: CONTINUED WITH MINI-FRAC JOB - USING CEMENT UNIT. PUMP RATE DECREASED TO 50 LPM Ø 345 BAR AFTER 6,6,M3 HAD BEEN BULLHEADED;LOW INFLOW RATE INDICATING THAT NO FRACTURE HAD BEEN CREATED.STOPPED PUMPING & RECORDED FALL-OFF PRESSURE." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CONTINUED BULLHEADING WITH 345 BAR. LOW PUMPING RATE = 4 LPM. PUMPED ANOTHER 0,8 M3 SEAWATER/POLYMER FLUID. STOPPED PUMPING - NO FRACTURE CREATED. MINI-FRAC JOB CONCLUDED." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: CLOSED LUBRICATOR VALVES & BLED DOWN ABOVE VALVES TO 0 BAR. RU PERFORATING BAR TOOLSTRING & ELECTRIC LINE TO PERFORATE ZONE #1B." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'workover -- perforate' and lasted for 4.0 hours. Operational details: RIH WITH ELECTRIC LINE + BAR. PERFORATED VIA TCP GUNS - USING BAR TO DETONATE - Ø 1513 HRS. PERFORATED FROM 3826 - 3865 M. POOH WITH BAR + ELECTRIC LINE." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'workover -- perforate' and lasted for 3.5 hours. Operational details: RD ELECTRIC LINE, LUBRICATOR & WIRELINE BOPS." "On 1997-10-29, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 3.5 hours. Operational details: OPENED WELL TO FLOW Ø 2051 HRS. FLOWED/TESTED WELL." "On 1997-10-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.0 hours. Operational details: FLOWED/TESTED WELL ON MAIN FLOW." "On 1997-10-30, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 18.0 hours. Operational details: FLOWED/TESTED WELL - ON MAIN FLOW PERIOD." "On 1997-10-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.0 hours. Operational details: FLOWED/TESTED WELL." "On 1997-10-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 8.5 hours. Operational details: FLOWED/TESTED WELL. TOOK PVT SAMPLES." "On 1997-10-31, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 9.5 hours. Operational details: SHUT-IN WELL BY CLOSING LPR-N/TESTER VALVE. CHECKED FOR LEAKAGE & THEN CLOSED FLOW WING VALVE ON FLOW-HEAD. BLED OFF PRESSURE DOWNSTREAM OF FLOW-HEAD. CLOSED CHOKE MANIFOLD. CONDUCTED DOWNHOLE PRESSURE BUILD-UP TEST." "On 1997-11-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.0 hours. Operational details: CONTINUED PERFORMING SHUT-IN BUILD-UP TEST." "On 1997-11-01, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 18.0 hours. Operational details: CONTINUED PERFORMING SHUT-IN BUILD-UP TEST." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.0 hours. Operational details: CONTINUED PERFORMING SHUT-IN BUILD-UP TEST." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: COMPLETED SHUT-IN BUILD-UP TEST." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: PRESSURED UP ON ANNULUS TO 200 BAR-LOCKED OPEN TESTER VALVE.PERFORMED MINI-FRAC TEST 2B. USING SEAWATER/POLYMER MIXTURE, THE FRACTURE CLOSURE PRESSURE WAS DETERMINED TO BE APPROXIMATELY 555 BAR AT 3045 M TVD - TOP PERFORATION." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CONTINUED WITH THE MINI-FRAC JOB. PUMPED 14,5 M3 OF 1,47 SG MUD. PUMP RATE = 1000 LPM AT 340 BAR." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: FLUSHED SURFACE TEST LINES & EQUIPMENT WITH SEAWATER.OPENED MPR & RELEASED RTTS W/13MT O/PULL.CLOSED MPR & SHEARED APR-RD VALVE W/300BAR ANNULUS PRESSURE. COMPLETED THE KILL PROCEDURE BY BULLHEADING 1,6 M3 1,47 SG MUD DOWN THE ANNULUS - FORCING FLUID BELOW PACKER TO BE BULLHEADED INTO FORMATION." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 3.5 hours. Operational details: OPENED MPR & CIRCULATED BOTTOMS UP - SHUTTING IN THE WELL & TAKING RETURNS THROUGH THE CHOKE LINE AFTER 2/3 ANNULAR VOLUME HAD BEEN PUMPED. MAX GAS READING = 3,7%. AFTER GAS DECREASED, OPENED WELL & CONTINUED CIRCULATING UP RISER - FOR A TOTAL OF 2 BOTTOMS UP." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3865m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: FLOW CHECKED & PUMPED SLUG." "On 1997-11-02, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3755m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 6.0 hours. Operational details: RD SURFACE FLOWHEAD. POOH/LD 5' LANDING STRING - LD 2 LUBRICATOR VALVES. STARTED LD SSTT-SUBSEA TEST TREE." "On 1997-11-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3755m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: COMPLETED LD SSTT." "On 1997-11-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2500m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 5.0 hours. Operational details: POOH - LD 3 1/2' TEST STRING. 125 JTS. LD AT REPORT TIME." "On 1997-11-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 317m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 8.0 hours. Operational details: FINISHED POOH WITH 3 1/2' TEST TUBING STRING. LD A TOTAL OF 358 JTS." "On 1997-11-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 6.0 hours. Operational details: LD DST BHA/TOOLS." "On 1997-11-03, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.0 hours. Operational details: CLEARED RIG FLOOR. MU CEMENTING STAND & TESTED TIW + LO-TORQ VALVES TO 345 BAR FOR 5 MINUTES. STAND SAME BACK." "On 1997-11-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1400m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.0 hours. Operational details: MU 7' EZSV & TIH USING 3 1/2' DP. 47 STANDS IN AT REPORT TIME." "On 1997-11-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3818m. The activity was categorized as 'plug abandon -- trip' and lasted for 11.0 hours. Operational details: COMPLETED TIH WITH 7' EZSV TO 3818 M." "On 1997-11-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3818m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.0 hours. Operational details: SET EZSV Ø 3818M. SHEARED SLEEVE W/18MT O/P; SET DOWN 18MT TO CONFIRM THAT EZSV WAS SET. STUNG OUT OF EZSV & TESTED EZSV TO 345 BAR FOR 15 MINUTES. STING BACK INTO EZSV & CLOSED UPPER ANNULAR IN PREPARATION FOR SQUEEZE JOB." "On 1997-11-04, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3818m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 5.0 hours. Operational details: WHILE TRANSFERRING CEMENT SPACER TO CEMENT UNIT, 3,5 M3 OF SPACER WAS ACCIDENTALLY TRANSFERRED TO ACTIVE SYSTEM. THE AMOUNT OF SPACER NEEDED FOR SQUEEZE JOB NOW NOT AVAILABLE. REBUILT THE SPACER. NOTE:CIRCULATED MUD AT 450 LPM - 130 BAR - WHILE REBUILDING THE SPACER CIRCULATED TOTAL OF 1,2 X BTMS UP." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3818m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 1.5 hours. Operational details: FINISHED RE-BUILDING CEMENT SPACER IN PREPARATION FOR SQUEEZE JOB. HELD PRE-JOB SAFETY MEETING ON RIG FLOOR WHILE SPACER WAS BEING WEIGHED UP. CLOSED UPPER ANNULAR & PRESSURED UP ON ANNULUS TO 60 BAR IN PREPARATION FOR SQUEEZE JOB." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3818m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 2.0 hours. Operational details: PERFORMED SQUEEZE JOB - SQUEEZING PERFS BELOW EZSV. PUMPED 3 M3 SPACER,4 M3 1,90SG CEMENT, 1,1 M3 SPACER & 7 M3 MUD;STUNG INTO EZSV & SQUEEZED 3 M3 CEMENT BELOW - FINAL SQUEEZE PRESSURE = 192 BAR Ø ,33 M3 PER MIN. SQUEEZED APPROX. 1,67 M3 CEMENT INTO PERFS. SHUT-DOWN-PRESSURE HELD Ø 135 BAR. WT. DOWN ON EZSV DURING JOB:10 MT." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3605m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: STUNG OUT OF EZSV & BLED OFF BACK-PRESSURE FROM ANNULUS. OPENED UPPER ANNULAR & SPOTTED 1 M3 CEMENT ON TOP OF EZSV. POOH TO 3605 M. TOC = PBTD = 3765 M." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3605m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: REVERSED OUT 1,5 X STRING VOLUME/670 LPM Ø 152 BAR. NO SPACER OR CEMENT IN RETURNS." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 3605m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: TESTED EZSV TO 345 BAR FOR 15 MINUTES USING UPR." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2325m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.0 hours. Operational details: PUMPED SLUG & POOH TO 2325 M ; LD 132 JTS. 3 1/2' DP ON TOH." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2325m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 3.0 hours. Operational details: CIRCULATED & INCREASED MUD WT. TO 1,55 SG." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: PUMPED SLUG & COMPLETED POOH WITH 7' EZSV MECHANICAL SETTING TOOL." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: MU FMC SPRING-LOADED TOOL & TIH TO WEAR BUSHING IN PREPARATION TO TEST BOPS." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: TESTED BOPS ON YELLOW POD - UPPER ANNULAR TESTED TO 20/241 BAR; LOWER ANNULAR + PIPE RAMS + FAIL SAFE VALVES TESTED TO 20/345 BAR. FUNCTION TESTED BOPS ON BLUE POD." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: POOH WITH SPRING-LOADED TOOL." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: CHANGED SAVER SUB ON TOP DRIVE FROM 3 1/2' IF TO 4 1/2' IF." "On 1997-11-05, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: RU & STARTED TESTING SURFACE EQUIPMENT." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: FINISHED TESTING 2 TOP DRIVE SAFETY VALVES + KELLY HOSE TO 20/345 BAR. RD TESTING EQUIPMENT." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: REPLACED 1 BENT JOINT OF 3 1/2' DP IN CEMENTING STAND & MOVED STAND IN DERRICK + LD 1 STAND 3 1/2' DP - TO ALLOW ACCESS TO 3 1/2' HWDP TO BE USED IN CUTTING BHA." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1200m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.5 hours. Operational details: MU BAKER 7' CASING CUTTING BHA + 3 1/2' HWDP. TIH WITH BHA ON 3 1/2' DP. 36 STANDS DP IN HOLE - AT APPROX. 1200 M - AT REPORT TIME." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2275m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.0 hours. Operational details: CONTINUED RIH W/ CSG CUTTING ASSY. SPACED OUT WITH SWIVEL IN WELLHEAD RECORDED PRESSURE AND TORQUE READINGS. START CUT AT 2275M." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2275m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: CONT 7' CSG CUT AND HAD 40 BAR PRESSURE DROP AND SLIGHT LOSS OF MUD. PULLED ABOVE CUT AND OBSERVED WELL IN 15 MIN. TRIP TANK GAINED 0,5 M3 WITH DECLINING RATE TO STEADY." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 160m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.0 hours. Operational details: PUMPED SLUG AND POOH. FLOW CHECKED BELOW BOP, OK." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: LAID DOWN 15 JT 3 1/2' HWDP AND CSG CUTTER ASSY." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: MADE UP SPRING ACTUATED TOOL AND RETRIEVED WEAR BUSHING." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 4.0 hours. Operational details: MADE UP FMC SPRING LOADED TOOL AND ATTEMPTED TO RETRIEVE SEAL ASSY WITH 15 TON DOWN WT AND 2700 DNM TORQUE. FLOW CHECKED AND PUMPED BTM UP OVER CHOKE. POOH, DID NOT RETRIEVE SEAL ASSY. RIH AND ATTEMPT TO RETRIEVE SEAL ASSY WITHOUT SUCCESS." "On 1997-11-06, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: MADE UP RUBBER NOSE JET SUB AND RIH TO SEAL ASSY AND WASH WELLHEAD WITH 1500 L/MIN AND 103 BAR. POOH." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: RIH AND ATTEMPT TO ENGAGE SEAL ASSY, NO GO. POOH." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: MODEFIED SPRING LOADED TOOL BY REMOVING LATCH LUGS AND GRIND OFF 4 MM. REDRESSED SAME." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: RIH AND ENGAGED SEAL ASSY. SET DOWN 5 TON, CLOSE L/ANNULAR FOR SUPPORT AND APPLIED 6000 DNM TORQUE, SET DOWN TO 14 TON DOWN WT AND PICKED UP NO INDICATION OF OVER PULL. CHECKED FOR FLOW, OPEN ANNULAR AND POOH. LAID DOWN SEAL ASSY AND RETRIEVING TOOL." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 106m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: MADE UP 7' CSG SPEAR/PACKOFF ASSY AND RIH TO WELLHEAD." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 105m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: ENGAGED SPEAR IN 7' CSG AND PULLED CSG FREE WITH 100 TON OVER PULL FLOW CHECKED WELL, WELL STATIC." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2169m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH WITH 7' CSG. RELEASED CSG SPEAR AND RACKED BACK IN DERRICK." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2169m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: RIG UP 7' CSG HANDLING EQUIPMENT." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 11.0 hours. Operational details: POOH AND LAID DOWN 179 JT 7' CSG." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: RIGGED DOWN CSG HANDLING EQUIPMENT AND CLEARED DRILLFLOOR." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: LAID DOWN CSG SPEAR ASSY." "On 1997-11-07, at Well NO 15/9-19 A, a drilling event occurred at a depth of 106m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: MADE UP WEAR BUSHING RUNNING TOOL, SET 10 3/4' WEAR BUSHING IN WELLHEAD. LAID DOWN RUNNING TOOL." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2210m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.5 hours. Operational details: MADE UP MULESHOE ON 3 1/2' DP AND RIH TO 2210M. BROKE CIRC AND GOT 12% GAS IN RETURN AT START OF CIRCULATION." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2210m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: FLOW CHECKED WELL, STATIC CONDITION. START CIRC 10 MIN AND GOT 38% GAS IN RETURNS. CLOSE ANNULAR AND INVESTIGATED FROZEN DP PRESSURE GAUGE ON CHOKE PANEL. STARTED TO CIRC BTMS UP WITH OPEN CHOKE." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2210m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: CONTINUED CIRCULATION THROUG OPEN CHOKE. GAS READING DECLINED TO 9% OPENED WELL AND CIRC LONG WAY UNTIL GAS STABILIZED AGAIN AT 9%." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2425m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: CONTINUED RIH TO 2425M. WASHED SECTION FROM 2205M TO 2275M PRIOR TO SET CMT PLUG." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2425m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.5 hours. Operational details: CIRCULATED AND CONDITION MUD 1,5 TIMES HOLE VOLUME. FLOW CHECKED, WELL STATIC." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2425m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: PUMPED 2 M3 HI-VIS PILL AND DISPLACED TO 2325M." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2325m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH TO 2325M. MADE UP CMT STAND W/VALVES AND CMT LINE." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2325m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: PUMPED 5,9 M3 SPACER WITH RIG PUMP AND TESTED CMT LINE TO 200 BAR." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2325m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: MIX AND PUMPED 5,4 M3 1,95 SG CMT SLURRY. DISPLACED WITH 6,55 M3 MUD TO SET PLUG. ESTIMATED TOC 2205M. ROTATED STRING WITH 70 RPM DURING JOB." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2205m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH TO 2205M." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2205m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: REVERSE OUT 1,2 TIMES PIPE VOLUME, NO CMT/SPACER OBSERVED. FLOW CHECKED, WELL STATIC." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2170m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.5 hours. Operational details: RACKED BACK CMT STAND AND POOH TO 2170M. CIRCULATED BTMS UP. MAX GAS 12%, DECLINED TO 2% AT END OF CIRULATION." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 1387m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: PUMPED SLUG AND POOH TO 1387M." "On 1997-11-08, at Well NO 15/9-19 A, a drilling event occurred at a depth of 450m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: LAID DOWN 3 1/2' DP." "On 1997-11-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: CONTINUED LAY DOWN 3 1/2' DP. TOTAL 147 JT. RIG DOWN 3 1/2' HANDLING EQUIPMENT." "On 1997-11-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.5 hours. Operational details: LAID DOWN CMT STAND. RIH AND LAID DOWN 4 3/4' DC. TOTAL 16 JT AT REPORT TIME." "On 1997-11-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: CONTINUED TO LAY DOWN EXCESS 4 3/4' DC'S, TOTAL 27 JT, CSG SCRAPER,BIT AND 3 JT 5' DP DUE TO WASHED OUT JT." "On 1997-11-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 2065m. The activity was categorized as 'plug abandon -- other' and lasted for 12.5 hours. Operational details: MADE UP RTTS TOOL AND RIH. START TO GET RESISTANCE AT 2070M, PULLED BACK TO 2065M AND SET RTTS. TEST 9 5/8' CSG WITH 180 BAR, OK. POOH AND LAID DOWN RTTS." "On 1997-11-09, at Well NO 15/9-19 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: SLIP AND CUT DRILLING LINE AND PRECAUTIONARY CHANGE WASH PIPE ON TOP DRIVE. TRANSFERED RIG TO WELL 15/9-19B AT 2200 HRS." "On 2013-11-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1403m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled with reduced rate from 1373m to 1403m with 3000-4010 liter/min, 50 % return of formation at 1380m, 155-237 bar, 122 rpm, 6-12kNm, ROP 2-5 m/hr, WOB 3-5 ton, ECD 1,438 sg. Max gas 0,04% Obtained surveys as required" "On 2013-11-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1484m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled from 1403m to 1484m with 4000 liter/min, 235 bar, 80-120 rpm, 12-25 kNm, ROP 27-29 m/hr, WOB 2-10 ton, ECD 1,420 sg. Max gas 0,05 %. Obtained surveys as required" "On 2013-11-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1484m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Recorded SCR`s." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1654m. The activity was categorized as 'drilling -- drill' and lasted for 8.2 hours. Operational details: Drilled 17 1/2' hole from 1484 m to 1654 m with 4000 liter/min, 235 bar, 138-142 rpm, 13-22 kNm, ROP 27-31 m/hr, WOB 3-8 ton, ECD 1,420-1,424 sg. Max gas 0,05%. Meanwhile picked up and racked back 13 3/8' casing in derrick." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1526m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.8 hours. Operational details: Circulated hole clean with 4500 liter/min, 280 bar. 3 x bottoms up. Racked back one stand each bottoms up." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1321m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH wet into 20' shoe with 17 1/2' BHA on 5 1/2' DP from 1443 m to 1321 m." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1321m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.0 hours. Operational details: Waited one weather. Monitored well on triptank. Observed loss rate of 150 liter/hour. Called in Ocean Price for cuttings discharge at 21:30 hrs. Meanwhile: Picked up and racked back 13 3/8' casing in derrick. Performed planned maintenance." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 1321 m to 1378 m. Unable to pass 1378 m. Established circulation with 2000-3300 liter/min, 77-165 bar, 5-15 rpm, 2-24 kNm, WOB 15-24 Ton. Worked string past 1378 meter." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1648m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 1378 m to 1648 m." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1654m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Washed down with 17 1/2' BHA from 1648 m to 1654 m at 3000 liter/min, 170 bar." "On 2013-11-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1670m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 17 1/2' hole from 1654 m to 1670 m with 4000 liter/min, 280 bar, 140 rpm, 11-21 kNm, ROP 31-36 m/hr, WOB 7-9 ton, ECD 1,420 sg. Max gas 0,04%. Meanwhile picked up and racked back 13 3/8' casing in derrick." "On 2013-11-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2002m. The activity was categorized as 'drilling -- drill' and lasted for 13.8 hours. Operational details: Drilled 17 1/2' hole from 1670 m to 2002 m with 4000-4430 liter/min, 260-282 bar, 140 rpm, 12-21 kNm, ROP 31-38 m/hr, WOB 1-12 ton, ECD 1,418-1,429 sg. Max gas 0,85%. At 13:30 the Ocean Pride disconnected cuttings hose due to bad weather. Meanwhile picked up and racked back 13 3/8' casing in derrick. Observed leaking pipe on ISO tank #3, stopped drilling." "On 2013-11-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1889m. The activity was categorized as 'interruption -- other' and lasted for 4.2 hours. Operational details: Repaired leaking pipe on ISO tank #3. Meanwhile: Circulated hole clean with 4500 liter/min, 280 bar. 3 x bottoms up. Racked back one stand each bottoms up." "On 2013-11-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1970m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Repaired leaking pipe on ISO tank #3. Meanwhile: RIH with 17 1/2' BHA from 1889 m to 1929. Established circulation with 500 liter/min, 5 bar, 30 rpm, 8 kNm. Reciprocated string between 1929 m and 1970 m." "On 2013-11-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2002m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Washed down with 17 1/2' BHA from 1970 m to 2002 m with 4450 liter/min, 292 bar, 140 rpm, 10 kNm." "On 2013-11-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2032m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 17 1/2' hole from 2002 m to 2032 m with 4450 liter/min, 296 bar, 140 rpm, 10-24 kNm, ROP 35-36 m/hr, WOB 3-6 ton, ECD 1,410 sg. Max gas 0,41%." "On 2013-11-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2032m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated hole clean with 4500 liter/min, 280 bar. 3 x bottoms up. Racked back one stand each bottoms up." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1929m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Circulated hole clean with 4500 liter/min, 280 bar. 3 x bottoms up. Racked back one stand each bottoms up." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1929m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flow check, ok." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1325m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH wet into 20' shoe with 17 1/2' BHA on 5 1/2' DP from 1929 m to 1325 m. Observed obstruction when passing 1378 meter with stabs, 10-15 Ton overpull. Ran back down to 1378 meter, sat down 15 Ton, not able to pass. Pulled back into shoe at 1325 meter." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1325m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.2 hours. Operational details: Waited one weather, not able to discharge cuttings to vessel due to hard weather. Monitored well on triptank." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1380m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Washed down with 17 1/2' BHA from 1366 m to 1404 m at 3000 liter/min, 132 bar, 15 rpm, 8-25 kNm. Observed 25 Ton WOB when bit passes 1378 m, continued to wash down. Observed 5-10 Ton WOB when stabs passes 1378 meter." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1370m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pulled back with 17 1/2' BHA on 5 1/2' DP from 1380 m to 1370 m. Observed obstruction when passing 1378 meter with stabs, 5-10 Ton overpull." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1384m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Slided down with 17 1/2' BHA from 1370 m to 1384 m at 3000 liter/min, 133 bar. Observed 20-21 Ton WOB when passes 1379-1382 m. Sat down 30 ton at 1395 meter, established rotation 15 rpm and attempted to wash down. No able to pass 1384 meter." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1325m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH wet into 20' shoe with 17 1/2' BHA on 5 1/2' DP from 1384 m to 1325 m." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1325m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.2 hours. Operational details: Waited one weather, not able to discharge cuttings to vessel due to hard weather. Monitored well on triptank. Vessel came alongside at 12:00 hrs. Commenced cuttings discharge from rig ISO tanks." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1392m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 17 1/2' BHA from 1364 m to 1376m. Sat down 30 Ton at 1376 meter. Established circulation with 500 liter/min, 45 bar, 15 rpm, 5-28 kNm. Washed past 1376 meter with bit and stabilizers to 1392 m." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1444m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Washed down from 1392 m to 1444 m with 4450 liter/min, 267 bar, 30-60 rpm, 10-25 kNm." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2013m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH with 17 1/2' BHA from 1444 m to 2013 m." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2030m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Washed down from 2013 m to 2030 m with 4450 liter/min, 285 bar, 140 rpm, 10-19 kNm." "On 2013-11-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2190m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: Drilled 17 1/2' hole from 2032 m to 2190 m with 4320 liter/min, 282-291 bar, 140 rpm, 15-22 kNm, ROP 32-36 m/hr, WOB 3-6 ton, ECD 1,42 sg. Max gas 0,2%." "On 2013-11-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2089m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: Circulated hole clean with 4330 liter/min, 277 bar. 3 x bottoms up. Racked back one stand each bottoms up." "On 2013-11-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2089m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile performed flowcheck, well static." "On 2013-11-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: POOH wet into 20' shoe with 17 1/2' BHA on 5 1/2' DP from 2089 m to 1362 m. Observed 5 - 8 t overpull at 1383 m bit depth. Built 13 3/8' casing stands and racked back same in derrick (47 stands racked in total)." "On 2013-11-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.8 hours. Operational details: Waited on weather/ISO tank vessel. Monitored well on trip tank. Meanwhile: Built 13 3/8' casing stands and racked back same in derrick (54 stands racked in total). Performed general rig maintenance." "On 2013-11-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1364m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: RIH w/ 17 1/2' BHA from 1362 m to 1384 m, 25 t down weight. Reamed from 1383 m to 1403 m w/ 3000 l/min, 170 bar, 25 RPM, 8-29 kNm. Backreamed interval. RIH f/ 1363 m to 1401 m, 25 t down weight. Reamed from 1401 m to 1405 m w/ 4000 l/min, 174 bar, 25 RPM, 8-19 kNm. Washed in f/ 1405 m to 1440 m, no restriction. Pumped OOH f/ 1440 m to 1403 m w/ 4000 lpm, 174 bar. POOH f/ 1403 m to 1362 m, 15 t drag at 1378 m, observed 1/4 turn on string. Wiped stand from 1363 m to 1403 m, no restriction. POOH from 1403 m to 1364 m into 20' shoe." "On 2013-11-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1364m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: Built 13 3/8' casing stands and racked back same in derrick (59 stands racked in total). Performed general rig maintenance." "On 2013-11-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1364m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: Isolated drill floor equipment and performed maintenance on fwd and aft PRS, TDS, block and dolly. Performed manriding in derrick after wind speed below 30 kts." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1364m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: Performed maintenance on fwd and aft PRS, TDS, block and dolly. Performed general rig maintenance." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1364m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: Troubleshot power supply issues on fwd PRS. De-isolated drill floor equipment. Built 13 3/8' casing stands and racked same in derrick (62 stands racked in total)" "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1593m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: Held TBT and removed FOSV from string. RIH w/ 17 1/2' BHA from 1364 m to 1502 m, 20 t down weight. Reamed in from 1502 m to 1593 m w/ 3000 lpm, 165 bar, 30 rpm and 10 - 20 kNm." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2190m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather/ISO tank vessel. Meanwhile: RIH from 1593 m to 2131 m. Filled pipe and established parameters. Down linked. Circulated B/U and reciprocated string f/ 2131 m - 2171 m, 3300 lpm, 185 bar, 80 rpm, 8 - 17 kNm. Connected ISO tank vessel and emptied 1/2 ISO tank on rig. Established drilling parameters and washed in from 2171 m to 2190 m" "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2285m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled 17 1/2' hole from 2190 m to 2285 m, average ROP: 17,3 m/hr, WOB 2 - 10 t. 4350 l/min/ 290 bar. 140 rpm / 10 - 24 kNm. ECD 1,42 SG. Reduced RPM to 80 while drilling through stringers. Performed surveys on connections as per DD instructions. Meanwhile built casing stands and shoe track. Racked same in derrick (all casing racked - in total 67 stands). Offloaded cuttings to vessel." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2331m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 17 1/2' hole from 2285 m to 2331 m, average ROP 23 m/hr, WOB 3 - 12 t. 4300 l/min/ 285 bar. 140 rpm / 10 - 24 kNm. ECD 1,42 SG." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2331m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2350m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 17 1/2' hole from 2331 m to 2350 m. Average ROP: 25,3 m/hr." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2350m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated B/U prior to drilling Balder Fm. w/ 4300 l/min/ 286 bar, 1,42 SG ECD. Took rotational check shots." "On 2013-11-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2355m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 17 1/2' hole from 2350 m to 2355 m, average ROP 20 m/hr. WOB 10 - 12 t. 4300 l/min/ 286 bar. 140 rpm / 15 - 22 kNm. ECD 1,42 SG." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2373m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 17 1/2' hole from 2355 m to 2373 m, average ROP: 24 m/hr. WOB 10 - 15 t. 4300 l/min/ 286 bar. 140 rpm / 15 - 22 kNm. ECD 1,42 SG." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2373m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Installed pressure gauge on TDS brake system to aid fault finding." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2418m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 17 1/2' hole from 2372 m to 2418 m, average ROP: 11,5 m/hr, WOB 12 - 19 t. 4300 l/min/ 286 bar. 80 - 140 rpm / 15 - 30 kNm. ECD 1,41 SG. Took surveys on connection as per DD instructions. Drilled hard stringers in interval." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2431m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 17 1/2' hole from 2418 m to 2431 m, average ROP: 7,5 m/hr, WOB 12 - 19 t. 4300 l/min/ 286 bar. 80 - 140 rpm / 15 - 30 kNm. ECD 1,41 SG. Took surveys on connection as per DD instructions. Drilled hard stringers in interval." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2493m. The activity was categorized as 'drilling -- drill' and lasted for 8.2 hours. Operational details: Drilled 17 1/2' hole from 2431 m to 2493 m, average ROP: 7,5 m/hr, WOB 8 - 16 t. 4300 - 4400 l/min/ 282 - 297 bar. 70 - 140 rpm / 8 - 28 kNm. ECD 1,41 SG. Took surveys on connection as per DD instructions. Drilled hard stringers in interval." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2493m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR's." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2493m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Observed leak on kelly hose at connection. R/B stand." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2493m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed PS21 slips, installed master bushing. M/U swedge and hose and lined up for circulation." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2493m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Prepared permits, isolated TDS and drawworks. Replaced damaged o-ring. Connected kelly hose and safety lines. De-isolated TDS and drawworks. Meanwhile circ. well with 1200 lpm / 51 bar." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2544m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed hose and circ. sub from string. M/U TDS, broke circulation. Tested kelly hose to 250 bar." "On 2013-11-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2544m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled 17 1/2' hole from 2493 m to 2544 m, average ROP: 10,7 m/hr, WOB 8 - 16 t. 4300 l/min/ 295 bar. 120 - 160 rpm / 12 - 28 kNm. ECD 1,41 SG. Took surveys on connection as per DD instructions. Drilled hard stringers in interval." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2573m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 17 1/2' hole from 2544 m to 2573 m, average ROP: 9,7 m/hr, WOB 6 - 15 t. 4300 l/min/ 295 bar. 140 - 160 rpm / 12 - 28 kNm. ECD 1,41 SG. Took surveys on connection as per DD instructions. Drilled hard stringers in interval." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2589m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 17 1/2' hole from 2573 m to 2589 m, average ROP: 8 m/hr, WOB 6 - 15 t. 4300 l/min/ 295 bar. 140 - 160 rpm / 12 - 28 kNm. ECD 1,41 SG." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 17 1/2' hole from 2589 m to 2595 m. Picked off bottom and downlinked. Diagnosed downhole tools with different parameters." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2618m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 17 1/2' hole from 2595 m to section TD at 2618 m. Average ROP: 7,6 m/hr. WOB 6 - 10 t. 4300 l/min/ 296 bar. 120 rpm / 16 - 28 kNm. ECD 1,41 SG." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2618m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.2 hours. Operational details: Circulated hole clean w/ 4330 l/min/ 295 - 285 bar, 120 RPM / 10 - 18 kNm, ECD 1,40 SG. Circulated total 3 B/U. Reciprocated string while circ. and R/B one stand after each B/U. Stopped rotation on last 30 min due to installation of sensor in TDS junction box (monitoring of brake system)." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2533m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Flowchecked, well static." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2333m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH wet w/ 17 1/2' BHA on 5 1/2' DP from 2533 m to 2333 m. Avg. tripping speed 400 m/hr." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2333m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped slug and allowed levels to stabilise." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2270m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH from 2333 m to 2270 m. Took 25 t overpull at 2270 m, attempted to wipe area 3 times, no success." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2260m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Rotated through tight spot from 2280 m to 2260 m w/ 15 RPM, 10 - 20 kNm." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1364m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH w/ 17 1/2' BHA on 5 1/2' DP from 2260 m to 1364 m. Avg. tripping speed 597 m/hr." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1364m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 10 min, well static. Performed trip drill." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH on 5 1/2' DP from 1364 m to 249 m. Avg. tripping speed 892 m/hr." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked prior pulling BHA through BOP. Well stable. Removed PS21 and installed bushings." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: R/B HWDP and DC, including jar and acc. Plugged into MWD and dumped data. L/D 17 1/2' BHA in three modules." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-11-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U Vetco bull nose jet sub. RIH to below BOP. Operated pipe rams." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Jetted BOP w/ 2000 lpm and 17 bar." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: P/U and M/U Vetco WBRRT. RIH on 5 1/2' HWDP. Jetted NSP area prior to landing WBRRT w/ 2200 lpm, 30 bar. RIH and landed WBRRT at 139,24 m (datum at 138,92 m), set down 6 t as per Vetco instructions. Pulled NSP free with 2 t overpull. Jetted NSP setting area w/ 2200 lpm, 30 bar." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Dropped 2 7/8' drift. POOH w/ WBRRT to surface. Inspected NSP, disengaged same from running tool. Re-set WBRRT and L/O same. L/O jetting assy and recovered drift." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor after wet trip." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT prior rigging up casing running equipment." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: R/U handling equipment for 13 3/8' casing: Removed drilling bails and elevator. Installed long bails. P/U Archer FAC tool. Changed out torque wrench die holders to be able to M/U fill up tool. M/U FAC tool and confirmed check valves open." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: TOFS: Cleaned and cleared rig floor." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: R/U handling equipment for 13 3/8' casing: Installed BX elevator, secured hoses and function tested same. Installed tilt arms on bails. Installed and function tested PS30 slips." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT prior to run casing stands from derrick." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 295m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 13 3/8' 72ppf Q125 Vam Top casing from surface to 295 m. Ran casing in stands from derrick, including shoe track. Average running rate 16 joints/hr. Float in self-fill mode." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 295m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Installed fill up tool. Evacuated rig floor due to excessive exhaust fumes from process turbines (Wind direction 284 deg)." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 13 3/8' casing in stands from 295 m to 1362 m. Average running rate 25 joints/hr." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke circ. w/ 220 l/min and 27 bar. Attempted to increase flow to 330 l/min, 36 bar, observed TDS weight decrease. Shut pumps down and bled pressure off." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: M/U swedge and circ. hose." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Attempted to breake circulation. Pressure increased to 70 bar, hold 3 min and bled off." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Evaluated situation and discussed way forward." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to pump down annulus. Pumped w/ 130 l/min, 10 bar, held 5 min. Pumped up to 15 bar, held 5 min. No pressure decrease, bled off pressure to zero." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up to pump down casing. Pressured up to 72 bar and observed sudden pressure drop. Float converted and ball sheared." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Increased flow in steps to 1500 l/min/ 30 bar. Circulated one casing volume (100 m3)." "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: R/D swedge and circ. hose" "On 2013-11-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2470m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: RIH with 13 3/8' 72ppf Q125 VamTop casing in stands from 1362 m to 2470 m. Filled casing every stand. Average running rate 25 joints/hr." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2470m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Changed handling equipment to 5 1/2'. L/O Weatherford elevator and Archer FAC tool. P/U and M/U 13 3/8' casing hanger and RT as per GE Vetco instructions." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2470m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed PS 30 and installed master bushing. Lowered hanger below rotary. Removed Weatherford casing tong." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 13 3/8' casing on 5 1/2' HWDP landing string from 2470 m to 2550 m. Performed break load transfer test on drawworks." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: M/U last stand HWDP. Filled string. RIH and circ. w/ 500 l/min, 11 bar. Set down 30 t weight at 2569,5 m. Attempted to pass restriction, pressure increased to 30 bar." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2610m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Picked up to above restriction. Increased flow in steps to 2000 l/min, 25 bar. Washed w/ 13 3/8' casing on 5 1/2' HWDP landing string from 2569 m to 2610 m w/ 2000 l/min/ 25 - 45 bar." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2612m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: P/U cement stand. M/U control lines and hoses. M/U cement stand to landing string. Washed down w/ 500 l/min, 9 bar and landed 13 3/8' casing hanger in 18 3/4' MS-700 wellhead at 2612,3 m." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2612m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Increased flow in steps to 2500 l/min/ 51 bar. Conditioned mud while circulating. Conducted TBT for cement job and tested cement hose prior to cement job. Circulated tot. 210 m3. No losses to formation." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2612m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Pumped 25 m3 1,60 sg spacer with 1900 l/min, 33 bar using rig pumps. Released bottom plug. Mixed and pumped 30 m3 1,92 sg slurry." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2612m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Displaced cement w/ 2500 l/min, 20 - 28 bar FCP. Bottom plug sheared w/ 130 bar and 7270 strokes (96% eff.). Continued to displace as per pump schedule. Bumped top plug after 8643 strokes (96% eff) w/ 100 bar. Held pressure for 2 min." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2612m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pressure tested casing to 285 bar/ 10 min. Volume pumped 1800 ltr, bled back 1800 ltr. Checked for backflow, ok." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Sat 13 3/8' seal assembly as per GE Vetco instructions. Applied 207 bar to annulus, held pressure for 10 min." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pressure tested surface line to 20/345 bar for 5/10 min." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Attempted to pressure test MS seal assembly to 20/345 bar for 5/10 min. Unable to get good test." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Opened annular and closed LPR. Re-tested MS seal assembly 20/345 bar 5/10 min, no success." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Released PADPRT as per GE Vetco instructions. L/D cement head. Installed sponge balls and circulated w/ 3000 l/min/ 30 bar, 2 x string volume." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with 5 1/2' HWDP landing string and PADPRT from 138 m to surface." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Inspected PADPRT and LIB. L/O running tool." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U annulus seal retrieval tool (ASRT)." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: RIH with ASRT. Engaged seal assembly with ASRT. Pressured up to 345 bar to enhance seal seating. Attempted to pressure test seal assembly to 345 bar / 5min. No success." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Evaluated situation. Discussed way forward w/ onshore organisation." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with ASRT and MS seal assembly from 138 m to surface." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Inspected MS seal assembly. Severe marks on seal body. Re-set and L/O ASRT." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U GE Vetco clean/flush tool." "On 2013-11-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH with flush tool. Washed 13 3/8' hanger, seal pocket and wellhead w/ 1700 l/min, 35 bar, 5-15 rpm." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Washed 13 3/8' hanger, seal pocket and wellhead w/ 1700 l/min, 35 bar, 5-15 rpm." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: POOH with clean and flush tool. L/O same." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: P/U and M/U PADPRT. Installed SG-TPR seal assembly on running tool. RIH and landed tool on hanger as per GE Vetco instructions. Set seal assembly." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lined up and performed line test 20/345 bar for 5/10 min." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Closed BOP and set seal assembly as per GE Vetco instructions. Held 207 bar for 10 min. Pressure tested seal assembly to 20/345 bar for 5/10 min. Evaluated test results and re-tested seal assembly to 345 bar." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Bled down pressure, opened BOP. POOH with PADPRT to surface, inspected tool and L/O same." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: P/U and M/U bull nose assembly. P/U and M/U wearbushing and wearbushing running/retrieval tool (WBRT)." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH and installed wearbushing." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Displaced BOP to seawater. Prepared to P/U isolation test tool." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Isolated equipment and inspected fwd PRS after contact w/ derrick structure." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Performed Statoil TOFS with drill crew #6 and third party personnel." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Electrician changed out drillers control joystick and re-calibrated same." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Released WBRT, L/O pup joint." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH with WBRT. Re- set retrieving tool and layed out same." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: P/U and M/U BOP isolation test tool (ITT). Function tested same." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: RIH w/ test tool, ran slowly past BOP as experienced hang-up. Landed BOP test tool in wellhead." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Flushed surface lines and confirmed line-up." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.2 hours. Operational details: Tested BOP to 20 bar/ 5 min and 345 bar/ 10 min." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Observed leak into string at test #4 while at 310 bar. Rigged down pump in sub and cmt hose. Opened BOP. Picked up ITT and relanded same in wellhead. Closed BOP and attempted to test, observed leak at 15 bar." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: POOH with ITT from 139 m to surface. Cleaned and inspected same. Hole in main seal." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Re-dressed test tool." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH with isolation test tool from surface to 139 m. Landed and set tool as per GE Vetco instructions." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: Lined up and continued testing BOP from test #4. Test pressure 20/345 bar for 5/10 min. Opened BOP, rigged down pump-in sub and hoses." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Held TBT prior to pulling test tool." "On 2013-11-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Released isolation test tool as per GE Vetco instructions. POOH ITT from 139 m to surface." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Inspected damaged seal on test tool. L/O same." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Cleared rigfloor of excessive equipment. Prepared for P/U 12 1/4' BHA." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: Flushed lines and tested BSR against casing. 20/285 bar for 5/10 min. Pumped 3840 ltr, bled back same volume. Meanwhile lifted BHA module #1 and #2 on HTS and worked on fwd PRS." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Displaced BOP back to OBM and filled lines." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed TBT prior to picking up BHA." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Function tested fwd PRS." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: P/U and M/U 12 1/4' BHA." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Plugged into tools and verified same." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 193m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: P/U and M/U 12 1/4' BHA including jar, DC and HWDP as per DD instructions. Installed totco ring on top of DC at 70,19 m." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1848m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: RIH w/ 12 1/4' BHA on 5 1/2' DP from 193 m to 1848 m. Avg. tripping speed 736 m/hr. Filled string at 1440 m." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1848m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Slew fault alarm on aft PRS. Attempted to clear fault w/o success." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: RIH on 5 1/2' DP from 1848 m to 2570 m, using fwd PRS. Avg. tripping speed 481 m/hr." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Closed BOP and performed choke drill w/driller, AD and lead driller." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2577m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Established parameters and washed from 2570 m to 2577 m w/ 2800 l/min, 185 bar, 30 RPM, 10 - 17 kNm." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2612m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Tagged TOC at 2577 m. Drilled shoetrack/cement from 2577 m to 2612 m. Average ROP: 8,2 m/hr, WOB 1 - 12 t. 3000 l/min/ 190 - 165 bar. 40 rpm / 12 - 17 kNm. ECD 1,35 - 1,31 SG. Reduced MW from 1,40 sg to 1,28 sg while drilling shoe track." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2613m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled out shoe. Observed frequent increase on WOB and pump pressure, worked string." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2623m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled and cleaned rat hole from 2612 m to 2618 m. WOB 2 - 5 t. 3300 l/min/ 205 - 185 bar. 80 rpm / 10 - 18 kNm. ECD 1,30 sg. Wiped every 2 m. Drilled 5 m new formation from 2618 to 2623 m." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2623m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pulled back into shoe with no flow and rotation. Hole in good condition." "On 2013-11-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2623m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: R/B one stand and circulated well prior to FIT w/ 3500 l/min/ 209 bar, 20 RPM, 1,30 sg ECD." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2623m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Spaced out and closed BOP. Confirmed line-up. Performed FIT to 1,55 sg EMW using 1,28 sg mud. Pumped 887 ltr from 5 bar to 65 bar at cement unit w/ 90 l/min. Bled back 835 ltr. Opened BOP." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2623m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2655m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 12 1/4' hole from 2623 m to 2655 m, average ROP: 12,8 m/hr. WOB 8 - 10 t. 3000 l/min/ 160 - 170 bar. 60 rpm / 16 - 22 kNm. ECD 1,31 sg. Drilled with reduced string rotation until top stab out of 13 3/8' casing. Bled in LCM mix as per procedure while drilling Ty Fm. Built 10 3/4' casing stands offline and racked same in derrick (3 stands racked in total)." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2655m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Tared CoPilot." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2708m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 12 1/4' hole from 2655 m to 2686 m, average ROP: 17,6 m/hr. WOB 7 - 12 t. 3500 l/min/ 218 bar. 120 rpm / 18 - 24 kNm. ECD 1,31 sg. Bled in LCM mix as per procedure while drilling Ty Fm. Built 10 3/4' casing stands offline and racked same in derrick (6 stands racked in total)." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2790m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 12 1/4' hole from 2686 m to 2790 m, average ROP: 34,6 m/hr. WOB 2 - 10 t. 3500 l/min/ 215 - 220 bar. 120 rpm / 18 - 22 kNm. ECD 1,31 sg. Bled in LCM mix as per procedure while drilling Ty Fm. Built 10 3/4' casing stands offline and racked same in derrick (9 stands racked in total)." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2856m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 12 1/4' hole from 2790 m to 2856 m, average ROP: 14,6 m/hr. WOB 8 - 15 t. 3500 l/min/ 218 - 225 bar. 120 rpm / 25 - 30 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 10 3/4'and 9 5/8' casing stands offline and racked same in derrick (14 stands racked in total)." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2897m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled 12 1/4' hole from 2856 m to 2897 m, average ROP: 12,6 m/hr. WOB 12 - 15 t. 3500 l/min/ 218 - 225 bar. 120 rpm / 25 - 30 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 9 5/8' casing stands offline and racked same in derrick (20 stands racked in total)." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2897m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR." "On 2013-11-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2961m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole from 2897 m to 2961 m, average ROP: 10,6 m/hr. WOB 11 - 14 t. 3500 l/min/ 215 - 225 bar. 120 rpm / 20 - 30 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 9 5/8' casing stands offline and racked same in derrick (30 stands racked in total)." "On 2013-11-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2998m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 12 1/4' hole from 2961 m to 2998 m, average ROP: 9,25 m/hr. WOB 11 - 14 t. 3500 l/min/ 215 - 225 bar. 120 rpm / 20 - 30 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 9 5/8' casing stands offline and racked same in derrick (35 stands racked in total)." "On 2013-11-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' hole from 2998 m to 3017 m, average ROP: 9,5 m/hr. WOB 11 - 14 t. 3500 l/min/ 215 - 225 bar. 120 rpm / 20 - 30 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 9 5/8' casing stands offline and racked same in derrick (37 stands racked in total)." "On 2013-11-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCRs." "On 2013-11-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3027m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 12 1/4' hole from 3017 m to 3027 m, average ROP: 13,3 m/hr. WOB 11 - 14 t. 3500 l/min/ 215 - 225 bar. 120 rpm / 20 - 30 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 9 5/8' casing stands offline and racked same in derrick (38 stands racked in total)." "On 2013-11-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3178m. The activity was categorized as 'drilling -- drill' and lasted for 10.2 hours. Operational details: Drilled 12 1/4' hole from 3027 m to 3178 m, average ROP: 14,7 m/hr. WOB 11 - 15 t. 3500 l/min/ 220 - 225 bar. 120 rpm / 20 - 35 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 9 5/8' casing stands offline and racked same in derrick (57 stands racked in total)." "On 2013-11-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3178m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCRs." "On 2013-11-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3260m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: Drilled 12 1/4' hole from 3178 m to 3260 m, average ROP: 12,6 m/hr. WOB 12 - 15 t. 3500 l/min/ 220 - 225 bar. 120 rpm / 20 - 30 kNm. ECD 1,30 sg. Added 4 sacks/stand to maintain background LCM particle concentration (Stealseal 100/400, Baracarb 50/150). Built 9 5/8' casing stands offline and racked same in derrick (63 stands racked in total). Repaired leakage in fwd hydraulic system manifold." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3299m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 12 1/4' hole from 3260 m to section TD at 3299 m, average ROP: 11,3 m/hr. WOB 12- 15 t. 3500 l/min/ 225 - 230 bar. 120 rpm / 25 - 36 kNm. ECD 1,30 sg. Built 9 5/8' casing stands offline and racked same in derrick (64 stands racked in total). P/U two intermediates w/ 2 centralizers and shoe joint. Built stand and racked same." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3300m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.2 hours. Operational details: Circulated hole clean w/ 3850 l/min/ 250 bar, 120 RPM / 20 - 25 kNm, ECD 1,30 sg. Reciprocated string. circulated in total 3 x B/U. P/U two joints w/ 2 centralizers and float collar joint. Built stand and racked same." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3299m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Flowchecked well on T/T. Observed 440 l/h losses." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3299m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Circulated w/ 3000 l/min/ 150 bar, 20 RPM / 17 kNm, 1,29 sg." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3299m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Initialized and dropped gyro as per Scientific Drilling instructions. Pumped tool down with 200 l/min, 9 bar." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 3299 m to 3100 m. Pulled wet and with restricted speed as per Scientific Drilling instructions." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pumped 3 m3 slug and chased same." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2575m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH on 5 1/2' DP from 3100 m to 2575 m. Avg. tripping speed 420 m/hr. Pulled with restriced speed due to drop gyro." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2575m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well inside shoe for 15 min, well static." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1808m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH on 5 1/2' DP from 2575 m to 1808 m. Avg. tripping speed 512 m/hr. Restricted speed and stoped for surveys as per Scientific instructions." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1929m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH on 5 1/2' DP from 1808 m to 2575 m. Took check surveys as per Scientific instructions." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 390m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH on 5 1/2' DP from 1929 m to 390 m. Avg. tripping speed 1231,2 m/hr." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 390m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: M/U TDS and took rotational survey as per Scientific instructions." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH from 390 m to 230 m." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min, well static." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Performed Statoil TOFS with drill crew #1 and third party personnel." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed auto slips and installed master bushing." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 85m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH from 230 m to 85 m and racked 5 1/2' HWDP." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 72m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: B/O double HWDP, recovered drop gyro. M/U stand and R/B same." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: L/D 12 1/4' BHA as per DD laydown plan." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Plugged in and downloaded data from BCPM and CoPilot." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: B/O and L/O module #4." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed TBT with new night shift for laying out BHA." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Layed out 12 1/4' BHA in modules from 33 m to surface." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U stand, made up jetting sub. M/U wearbushing running and retrieval tool (WBRRT)." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH w/ WBRRT, landed same and set down 5 - 7 t as per Vetco instructions. Released wearbushing w/ 40 t overpull." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Racked stand, M/U TDS. Flushed wellhead with 2000 l/min, 30 bar." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 46m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Dropped 3' drift for landing string. POOH with WBRRT to surface." "On 2013-11-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 46m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Inspected wearbushing, released/re-set RT and L/O same." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with jet sub, L/O same. Cleared rig floor." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for rigging up casing handling equipment." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: R/U handling equipment for 9 5/8' casing. Installed fill-up tool and elevator. Moved Weatherford casing tong into position, connected and function tested same. Removed master bushing and installed PS30 slips." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT with all involved personnel for M/U shoe track stands from derrick and P/U 9 5/8' casing joints from deck." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 74m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: P/U 9 5/8' shoe stand from derrick and RIH same. Verified floats holding. P/U landing collar stand from derrick and M/U same to shoe stand. Thread locked stands. RIH to 74 m." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 VamTop casing from 74 m to 350 m. Filled casing while running in. Average running rate 7,1 joints/hr." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT with day shift for running casing." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 571m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 VamTop casing from 350 m to 571 m. Filled casing while running in. Average running rate 9 joints/hr." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1562m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 VamTop casing stands from 571 m to 1562 m. Filled casing every stand while RIH. Average running rate 30 joints/hr." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2600m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 VamTop casing stands from 1562 m to 2690 m. Filled casing every stand while RIH. Average running rate 34 joints/hr." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2690m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed to 10 3/4' elevator inserts. P/U X-O stand and M/U same. Changed slips inserts and casing tong to 10 3/4'." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 10 3/4' 65,7 ppf P110 VamTop casing stands from 2690 m to 3146 m. Filled casing every stand while RIH. Average running rate 22 joints/hr." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Filled casing, removed fill-up tool. Removed casing elevators and installed DP elevator." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U and M/U 10 3/4' casing hanger. Removed protection and inspected hanger." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3158m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed casing slips. RIH w/ casing hanger from 3146 m to 3158 m. Installed master bushings." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3158m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: R/D casing tong." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3158m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT with night shift to run and land casing on HWDP LS." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3280m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 10 3/4' x 9 5/8' casing on 5 1/2' HWDP landing string from 3158 m to 3280 m. Up weight 300 t, down weight 195 t. Circulated last stand w/ 500 lpm and 22 bar." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3280m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: P/U cement head. M/U cement hoses. M/U cement head to landing string." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3296m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Broke circ. w/ 500 l/min and 22 bar. RIH and landed 10 3/4' casing hanger in MS 700 wellhead. Set down casing weight, marked pipe and confirmed stem free as per GE Vetco instructions." "On 2013-11-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3296m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Increased flow in 250 l/min steps to 1700 l/min/ 46 bar. Observed loss tendency, 2,5 m/h. Reduced pump rate to loss free rate at 1600 l/min/40 bar. Conditioned mud while circ. until MW in/out 1,28 sg." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3296m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Circulated w/ 1600 l/min/40 bar. Conditioned mud while circ. until MW in/out 1,28 sg. Held TBT for cement job while circ." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3296m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Verified line-up for cement job. Pumped 22 m3 1,60 sg spacer w/ 1600 lpm, 41 - 32 bar. Released dart for bottom wiper plug. Mixed and pumped 15 m3 of 1,90 sg slurry at 650 l/min. Observed bottom plug shear after 1000 l pumped. Displaced cement to rig floor w/ 800 liters FW. Released top dart and pumped 1,5 m3 FW from cement unit. Observed top plug shear w/ 88 bar after 900 l." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3269m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Displaced cement as per pump schedule using rig pumps at 1600 l/min. Bumped and sheared bottom plug w/ 1000 l/min and 5758 strokes. shear pressure 130 bar. Continued displacing cement w/ 1600 l/min, 50 - 68 bar. Reduced rate to 500 l/min, 50 bar for last 2 m3. Bumped top plug after 5476 strokes (96,4% eff). Pressured up to 120 bar, held for 3 min. Lost 3 m3 during cement job." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3296m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up to cement unit, equalized pressures. Tested 9 5/8' x 10 3/4' casing to 20/345 bar for 5/10 min." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3296m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Bled down pressure, disconnected cement hose and checked for back flow. Non observed." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Released RT. L/D cement head. Installed sponge balls and circulated w/ 2200 l/min/ 13 bar." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: POOH with 5 1/2' HWDP landing string and RT from 140 m to surface." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Removed seal assembly from PADPRT and L/O same. No damage on seal assembly. Cleaned rig floor." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 40m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: M/U jetting sub assembly and RIH from surface to 40 m." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: P/U and M/U wearbushing and wearbushing running/retrieval tool (WBRRT). RIH from surface to 140 m and landed wearbushing. POOH to surface with running tool." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Layed out WBRRT. Cleaned and cleared rig floor." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: P/U BOP isolation test tool (ITT). Changed seals on tool." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: RIH w/ test tool. M/U TDS and landed BOP test tool in wellhead as per GE Vetco instructions." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Flushed drill floor manifolds to water." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Attempted to test BOP. Observed fluid coming up string." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: Released test tool and POOH. Inspected and L/D same." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: P/U WBRRT, RIH and pulled wearbushing w/ 40 t overpull. Jetted WH area with 1800 l/min, 17 bar. POOH from 140 m to surface." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Attempted to release wearbushing from RT, no success. Layed out in one piece." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: P/U PADPRT, installed seal assembly. RIH and landed tool at 140 m in 10 3/4' hanger." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Lined up for bullheading B-annulus to brine. Bullheaded 1,09 sg brine as per program, pumped 85 m3 brine followed by 28 m3 SW. Stopped pumping and monitored pressure for 15 min, 96 - 89 bar." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Bled of pressure in steps from 89 bar to 73 bar, bled back 8 m3. Monitored pressure development, decreased from 73 - 65 bar in 60 min." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Bled down pressure in 2m steps from 65 bar to 34 bar, bled back 10 m3." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Bullheaded well with SW, 250/500/1000 l/min with 33/75/94 bar, pumped 28 m3." "On 2013-11-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Monitored pressure after bullheading, pressure decreased from 83 bar to 73 bar." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: Bled down pressure in 2m steps from 73 bar to 0 bar. Shut in, monitored pressure built up to 20 bar/10 min. Opened well and observed on T/T, 0,6 m3 returns. Shut in, monitored pressure built up to 7 bar/10 min. Opened well, 0,2 m3 /10 min. Shut in, no pressure increase observed. Bled back 12,5 m3 in total, leaving 83,5 m3 brine in the annulus." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.8 hours. Operational details: Set and energized seal assembly as per GE Vetco procedure. Performed line test and attempted to pressure test seal assembly to 20/345 bar for 5/10 min. No success." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Released seal assembly running tool." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared to displace riser to 1,28 SG OBM." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared and displaced riser to 1,28 SG OBM with 2000 lpm, 10 bar." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to POOH with PADPRT." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH with PADPRT from 140 m. Cleaned and inspected PADPRT, L/D same." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor of excess equipment." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: M/U jetting assy and RIH to 45 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: P/U and M/U seal assembly retrieving tool." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with seal assembly retrieving tool to 140 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Landed and set seal assembly retrieving tool according to Vetco instructions." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pressure tested seal assembly to 20/345 bar for 5/10 min." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.8 hours. Operational details: Tested BOP pipe rams and annular to 20/345 bar for 5/10 min. Tested kill and choke lines to 20/345 bar for 5/10 min." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Realeased seal assembly retrieving tool according to Vetco instructions." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: POOH seal assembly retrieving tool/BOP test tool from 140 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Cleaned and inspected seal assembly retrieving tool and L/D same." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: M/U wear bushing running tool and wear bushing. RIH with wear bushing 140 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Set wear bushing and released running tool." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH with wear bushing running tool from 140 m. L/D WBRT." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Tested BOP shear rams and 9 5/8' casing to 20/345 bar for 5/10 min." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting Prior to M/U 8 1/2' BHA." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: P/U and M/U 8 1/2' auto trak assy to 28 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Plugged into auto trak, program and verify tool for correct setup." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: M/U 8 1/2' BHA and RIH to 47 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to handling of radioactive sources." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Installed radioactive sources into litmotrak." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed handling equipment from 5' to 5 1/2'." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 89m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: M/U 8 1/2' BHA and RIH from 47 m to 89 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 89m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed handling equipment from 5 1/2' to 5'." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 182m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: P/U X-O and jar. RIH with 8 1/2' BHA on 5 1/2' HWDP from 89 m to 182 m." "On 2013-11-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 182m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: R/U test line to TDS. Performed line test to 20 /345 bar for 5/10 min. Pressure tested TDS and kelly hose to 20/345 bar for 5/10 min." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 182m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Installed PS-21 slips." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 182 m to 1000 m." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Filled string. Performed shallow test on MWD tool with 2000 lpm, 128 bar." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed PS-21 slps from rotary. Performed kick drill with crew." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to performing slip/cut drill line." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Performed slip/cut 34 m drill line. Cleaned and cleared rig floor. Calibrated drawworks and reset crown o matic." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2260m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 1000 m to 2260 m. Filled drill string every 1000 m." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3209m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 2260 m to 3209 m. Filled drill string every 1000 m." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3209m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed choke drill with crew. Closed annular and applied 30 bar on casing. Started up pump in steps to kill speed holding casing pressure constant. Reduced pump to zero strokes holding constant casing pressure 30 bar. Bled off casing pressure to zero. Opened annular." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3250m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Washed down with 1000 lpm, 63 bar, from 3209 m to 3250 m. Tagged top of cement with 4 ton @ 3250 m." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3250m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took up/down weight, 169/124 ton. Down-link MWD tool." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3252m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drill out plug and FC from 3250 m to 3252 m with 1600 lpm, 122 bar, 100 rpm, 16-22 kNm, 1-3 ton WOB. Weighted up mud to 1,32 SG." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3295m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled shoetrack/cement from 3252 m to 3295 m with 2000 lpm, 162 bar, 90 rpm, 16-23 kNm, 1-4 ton WOB." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3299m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Washed and cleaned rat hole in 2 m steps from 3295 m to 3299 m with 2000 lpm, 161 bar, 80 rpm, 15-21 kNm, 1-4 ton WOB. No cement." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3302m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 3 m new formation from 3399 m to 3302 m with 2000 lpm, 161 bar, 80 rpm, 15-21 kNm, 1-4 ton WOB. ECD 1,47 SG Max gas: 0,02 %." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3295m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pulled back into 9 5/8' shoe at 3295 m." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3295m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated well clean and conditioned mud weight to 1,32 SG with 2450 lpm, 220 bar. ECD 1,43 SG Max gas: 0,02 %." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3295m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Lined up for FIT test and confirmed correct line up. Spaced out and closed ram. Performed FIT to 1,60 SG using 1,32 SG mud. Pumped 930 ltr and blead back 915 ltr" "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3295m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: B/O 1 wild single of 5 1/2' pipe from drill string. Serviced TDS, topped up gear box with 40 ltr oil." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3295m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Decoded signals from MWD. Took SCR @ 3295 m, 1,32 SG. Pump 1 20/30/40 stroke, 33/41/42 bar. Pump 2 20/30/40 stroke, 22/32/44 bar." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3313m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drill 8 1/2' hole from 3302 m to 3313 m with 2400 lpm, 209 bar, 80 rpm, 17-25 kNm, 10 ton WOB. ROP 18 m/hr. ECD 1,50 SG. Max gas: 0,02 %." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3313m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Picked up of bottom, spaced out for BOP. Performed flow check. well static." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3370m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled 8 1/2' hole from 3313 m to 3370 m with 2400 lpm, 202 bar, 160 rpm, 18-26 kNm, 7 ton WOB. ROP 10 m/hr. ECD 1,50 SG. Max gas: 0,03 %. Down link and take survey after connection." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3370m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Reamed single from 3370 m to 3357 m. Tare co-pilot." "On 2013-11-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3410m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8 1/2' hole from 3313 m to 3370 m with 2400 lpm, 209 bar, 160 rpm, 18-28 kNm, 6-7 ton WOB. ROP 10-25 m/hr. ECD 1,51 SG. Max gas: 0,05 %. Down link and take survey after connection." "On 2013-11-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3496m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled 8 1/2' hole from 3370 m to 3496 m with 2400 lpm, 202 bar, 120 rpm, 16-23 kNm, 7 ton WOB. ROP 10 m/hr. ECD 1,51 SG. Max gas: 0,8 %. Reduced ROP to 10 m/hr @ 3471 m to 3496 m. Down link and take survey after connection." "On 2013-11-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3499m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 8 1/2' hole from 3496 m to 3499 m. with 2400 lpm, 211 bar, 120 rpm, 16-25 kNm, 5 ton WOB. ROP 25-30 m/hr. ECD 1,52 SG. Max gas: 2,77 %. Down link and take survey after connection." "On 2013-11-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3532m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 8 1/2' hole from 3499 m to 3532 m. with 2400 lpm, 212 bar, 120 rpm, 22-27 kNm, 4 ton WOB. ROP 25-30 m/hr. ECD 1,52 SG. Max gas: 1,9 %. Down link and take survey after connection." "On 2013-11-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3532m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 3532 m, 1,32 SG. Pump 1. 20/30/40 stroke, 33/41/42 bar. Pump 2. 20/30/40 stroke, 22/32/44 bar." "On 2013-11-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3730m. The activity was categorized as 'drilling -- drill' and lasted for 8.5 hours. Operational details: Drilled 8 1/2' hole from 3532 m to 3730 m. with 2400 lpm, 218 bar, 120 rpm, 18-27 kNm, 3-5 ton WOB. ROP 25-30 m/hr. ECD 1,53 SG. Max gas: 2,16 %. Down link and take survey after connection." "On 2013-11-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3730m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 3730 m, 1,32 SG. Pump 1. 20/30/40 stroke, 28/37/49 bar. Pump 2. 20/30/40 stroke, 27/38/50 bar." "On 2013-11-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3912m. The activity was categorized as 'drilling -- drill' and lasted for 7.8 hours. Operational details: Drilled 8 1/2' hole from 3499 m to 3532 m. with 2400 lpm, 228 bar, 120 rpm, 22-30 kNm, 4-9 ton WOB. ROP 25-30 m/hr. ECD 1,53 SG. Max gas: 2,51 %. Down link and take survey after connection." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3954m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8 1/2' hole from 3912 m to 3954 m. with 2400 lpm, 219 bar, 120 rpm, 17-25 kNm, 5 ton WOB. Avg ROP 24 m/hr. ECD 1,60 SG. Max gas: 2,95 %. Down link and take survey after connection." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3954m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: At 3954 m observed STDP increased from 220 bar to 245 bar and WOB increased from 4 ton to 9 ton. Drillstring stalled out. Attempted to regain rotating no success. Pulled 70 ton overpull on drillstring, string free. Back reamed 1 single prior to commence drilling." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3974m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 8 1/2' hole from 3954 m to 3974 m. with 2400 lpm, 220 bar, 120 rpm, 18-23 kNm, 4 ton WOB. Avg ROP 16 m/hr. ECD 1,51 SG. Max gas: 0,8 %. Down link and take survey after connection. Back reamed stand prior to connection." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4025m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 8 1/2' hole from 3974 m to 4025 m. with 2400 lpm, 220 bar, 120 rpm, 18-23 kNm, 4-5 ton WOB. Avg ROP 22 m/hr. ECD 1,53 SG. Max gas: 3,0 %. Down link and take survey after connection." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4052m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 8 1/2' hole from 4025 m to 4052 m. with 2400 lpm, 226 bar, 120 rpm, 22-26 kNm, 5 ton WOB. Avg ROP 22 m/hr. ECD 1,53 SG. Max gas: 2,4 %. Down link and take survey after connection." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4052m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 4052 m, 1,32 SG. Pump 1. 20/30/40 stroke, 33/41/54 bar. Pump 2. 20/30/40 stroke, 34/40/51 bar." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4337m. The activity was categorized as 'drilling -- drill' and lasted for 12.5 hours. Operational details: Drilled 8 1/2' hole from 4052 m to 4337 m. with 2400 lpm, 238 bar, 140- 160 rpm, 20-28 kNm, 4-6 ton Avg WOB. ROP 23 m/hr. ECD 1,56 SG. Max gas: 2,9 %. Down link and take survey after connection." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4337m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 4337 m, 1,32 SG. Pump 1. 20/30/40 stroke, 34/43/55 bar. Pump 2. 20/30/40 stroke, 36/43/53 bar." "On 2013-11-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4434m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 8 1/2' hole from 4337 m to 4434 m. with 2400 lpm, 236 bar, 160 rpm, 24-30 kNm, 4-5 ton WOB. Avg ROP 26 m/hr. ECD 1,56 SG. Max gas: 2,6 %. Down link and take survey after connection." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4563m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole from 4434 m to 4563 m. with 2400 lpm, 240 bar, 160 rpm, 24-30 kNm, 4-5 ton WOB. Avg ROP 21 m/hr. ECD 1,57 SG. Max gas: 2,4 %. Down link and take survey after connection." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4685m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole from 4563 m to 4685 m. with 2420 lpm, 248 bar, 180 rpm, 24-30 kNm, 4-7 ton WOB. Avg ROP 20 m/hr. ECD 1,59 SG. Max gas: 2,0 %. Down link and take survey after connection." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4685m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated hole clean with 2425 lpm, 248 bar, 180 RPM, 24-29 kNm, ECD 1,55 SG Circulated total 1,5 B/U. Reciprocated drill string from 4680 m to 4660 m." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4685m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Attempted to rack back stand no success. Unable to back out due to TDS brake. Troubleshot on TDS brake system. Spanned out stand with iron roughneck. R/B stand in derrick. M/U circulation swedge and hose to dril string. Circulated on well with 660 lpm, 48 bar. Restarted TDS all functions returned to normal. Broke out circulation swedge." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4620m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Connected TDS to drill string. Circulated hole clean with 2425 lpm, 248 bar, 180 RPM, 24-29 kNm, ECD 1,54 SG Circulated total 3,5 B/U while reciprocated drill string and racked one stand per btm's up." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4661m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took torque readings." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4661m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. Well static." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4661m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Established with 2400 lpm, 235 bar, 20 rpm, 18-22 kNm. Down link to ribs off." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4620m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 8 1/2' BHA from 4661 m to 4620 m. Unable to function mudbucket." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4620m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Troubleshot on interlock system for mudbucket. Meanwhile circulated with 1800 lpm and 60 rpm. Reciprocated drill string." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4376m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 8 1/2' BHA from 4620 m to 4376 m wet. Drag seen @ 4593 m, 25 ton. Pumped through tight spot @ 4593 m." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4336m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Re log area from 4376 m to 4336 m with 60 m/hr, 1800 lpm and 60 rpm." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4336m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took up/down weight, 195/139 ton." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4336m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. well static." "On 2013-12-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4336m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 4 m3 0f 1,61 SG slug." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3288m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: POOH with 8 1/2' BHA from 4336 m to 3288 m. Avg. tripping speed 322 m/hr." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3288m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well. Well static. Took torque readings." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1922m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 8 1/2' BHA from 3388 m to 1922 m. Avg. tripping speed 651 m/hr." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' BHA from 1922 m to 1360 m. Avg. tripping speed 562 m/hr." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job/handover meeting with crew." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned and checked BX-elevator. Cheched oil level on HPU and top up same." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 223m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 8 1/2' BHA from 1360 m to 223 m. Avg. tripping speed 758 m/hr." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 223m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Performed kick drill with crew, 65 sec." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 223m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. Well static." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 8 1/2' BHA from 223 m to 100 m." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to handling BHA and radioactive sources." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed to 5' handling equipment. Filled trip tank." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' BHA from 100 m to 48 m while R/B 5 1/2' HWDP and jar in derrick." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed radioactive sources from Litro rak." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Plugged in to MWD and down loaded data." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH with 8 1/2' BHA from 48 M and L/D same on deck." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and clered rig floor for excess equipment." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rig 7' liner equipment." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: R/U handling equipment for 7' liner. CSG tong, inserts in BX-elevator, Installed fill up swedge to TDS. Pulled in HTS and installed power rollers on same." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Performed service on traveling bluck, electric motor and dolly." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: R/U handling equipment for 7' liner. Installed PS-30 in rotary. M/U swedge to TIW. Checked CSG tong." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to P/U and run 7' liner." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: M/U shoetrack to 60 m. P/U 7' primary shoe joint, checked float. M/U shoe joint, intermediate joints and float collar joint, checked flow through. Filled every joint." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Weatherford casing crew installed hydraulic hoses for stabbing arm and changed out sticking inserts in BX-elevator from Weatherford to Mearsk inserts." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Pulled up joint no. 6 attempted to M/U same no success. Troubleshooting on Weatherford casing tong. Found damaged/sheared breakband." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to change out damaged breakband." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed out damaged breakband." "On 2013-12-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Back out joint no. 6 and confirmed threads damaged on joint and in collar on float joint pup." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: L/U 7' liner joint no. 155 due to damaged threads." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Attempted to break out collar on float pup, no success due to missing jaws size for breaking out collars." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: L/O primary landing/float joint. Backed out with chain tongs." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Checked box on intermediate joint no. 4 threads ok." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U back up landing coller/float joint B. Attempted to M/U with Weatherford casing tong no success." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Weatherford casing crew changed dies and attempted to solve the problem." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to R/D casing tong." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: L/U landing collar/float joint." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Prepared to R/D Weatherford casing tong. Removed HTS rollers and frame." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Removed casing tong from frame and transferred casing tong to deck." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U back up casing tong from deck." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to R/U Weatherford back up casing tong." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: R/U Weatherford back up casing tong." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to run 7' liner." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: P/U and M/U landing collar/float joint. RIH with 7' liner from 60 m to 107 m. Filled every joint." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 107m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed casing tong dies." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 7' liner from 107 m to 118 m. Filled every joint." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed Time out for safety regarding red zone policy." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Changed liner running setup to using PRS." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 118m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Function tested Weatherford auto stabber." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor. Held TOSF." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 259m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: RIH with 7' liner from 118 m to 259 m. Filled every 5th joint. Average running rate 3 joints/hr. L/U damaged/over torqued joint no. 147 and 148." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 259m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job/handover meeting with crew." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 328m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 7' liner from 259 m to 328 m. Filled every 5th joint. Average running rate 6 joints/hr." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 328m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed casing tong dies and clamps." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 328m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Attempted to change collar on joint no. 130 no success due to spear collar not compatible. L/U damaged/over torqued joint no. 130 and 131." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 411m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 7' liner from 328 m to 411 m. Filled every 5th joint. Average running rate 3,5 joints/hr." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 411m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed casing tong dies." "On 2013-12-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 423m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 7' liner from 411 m to 423 m. Filled every 5th joint. Average running rate 4 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 470m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 7' liner from 423 m to 470 m. Filled every 5th joint. Average running rate 8 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 470m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed casing tong dies." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 610m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 7' liner from 470 m to 610 m. Filled every 5th joint. Average running rate 8 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 610m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed casing tong dies." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 873m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 7' liner from 610 m to 873 m. Filled every 5th joint. Average running rate 7 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 873m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Grease and checking elevator, slips and casing tong." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 884m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 7' liner from 873 m to 884 m. Filled every 5th joint. Average running rate 3,5 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 884m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Planned to P/U liner hanger, due to bad weather forecast." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 884m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to P/U and R/B liner hanger in derrick." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 884m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U liner hanger from deck and R/B same in derrick. Tested ran cement head with PDM. Checked dies in PRS." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1060m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 7' liner from 884 m to 1060 m. Filled every 5th joint. Average running rate 6,5 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1060m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned rig floor." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1084m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 7' liner from 1060 m to 1084 m. Filled every 5th joint. Average running rate 7 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1084m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Changed casing tong dies." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1084m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: Performed derrick inspection and looking for PDO due to bad weather forecast. Observed loose rollers on fast line guide. Removed fast line guide from derrick. Checked work site for tools." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1164m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 7' liner from 1084 m to 1164 m. Filled every 5th joint. Average running rate 4,5 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1164m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed casing tong dies." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1211m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 7' liner from 1164 m to 1211 m. Filled every 5th joint. Average running rate 4 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1211m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed out casing tong dies and holders prior to M/U 7' pup joint." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1356m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 7' liner from 1211 m to 1356 m. Filled every 5th joint. Average running rate 8 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1356m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed casing tong dies." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1402m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 7' liner from 1356 m to 1402 m. Filled every 5th joint. Average running rate 5 joints/hr." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1402m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed casing tong dies." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1503m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 7' liner from 1402 m to 1503 m. Filled every 5th joint. Average running rate 5 joints/hr. Broke out joint no. 122 checked thread due to bad graph, thread cleaned and inspected ,thread ok." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1503m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to M/U liner hanger." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1503m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Changed to 5 1/2' inserts in BX-elevator. P/U and M/U liner hanger." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1503m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to remove PS-30 slips and install master bushing in rotary." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1503m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor for excess liner equipment." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1503m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed PS-30 slips and install master bushing in rotary." "On 2013-12-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1515m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Lowered liner hanger and removed protection covers." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1515m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: R/D casing tong." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1515m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Filled PBR with warter simultaneously circulated liner volume, 880 lpm, 60 bar according to weatherford instructions." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1515m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed PS-21 in rotary." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1730m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 7' liner on 5 1/2' HWDP from 1515 m to 1730 m. Average running rate 7 stands/hr." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1730m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Filled pipe." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2560m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with 7' liner on 5 1/2' DP from 1730 m to 2560 m. Filled every 5th stands. Average running rate 7,5 stands/hr." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2889m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 7' liner on 5 1/2' DP from 2560 m to 2889 m. Filled every 5th stands. Average running rate 6,5 stands/hr." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2889m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.8 hours. Operational details: Waited on weather. Connected TDS to drill string. Broke circulation, circulated 1x liner volume 30 m3 with 440 ltr, 55 bar. Recordet rotating torque with 20 rpm, 15 kNm, 150 ton. Took up/down weight, 180/130 ton." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2889m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Waited on weather. Monitored well on trip tank. Broke circulation every 2 hrs. Pressure tested mud hoses. Housekeeping in sack store and heavy tool store. Electrician inspected Drawworks. Cleaned in pump room and pit room. Crew partake in E-learning course." "On 2013-12-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2889m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waited on weather. Established circulation with 450 lpm, 55 bar. Circulated and conditioned mud prior to RIH with liner. Circulated 1x btm's up." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2889m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.8 hours. Operational details: Waited on weather. Circulated and conditioned mud with 450 lpm, 50 bar prior to RIH with liner. Circulated 1x btm's up." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2889m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waited on weather. Lined up on trip tank and observed well. Broke circulation every 2 hrs. Evaluated weather conditions 60 kt. Prepared to start RIH with 7' liner." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2889m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather. Performed pre job meeting with crew prior to start RIH with 7' liner on 5 1/2' DP." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3091m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 7' liner on 5 1/2' DP from 2889 m to 3091 m. Filled every 5th stands. Average running rate 7,5 stands/hr." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3091m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to perform derrick inspection and RIH 7' with 7' liner on 5 1/2' DP." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3091m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Performed Inspection of derrick and drill floor areas. Removed lose gate and post at drawworks area, and secured handrail at monkey board level." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3290m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 7' liner on 5 1/2' DP from 3091 m to 3290 m. Filled every 5th stands. Average running rate 6,5 stands/hr." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3290m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Took torque and drag readings prior to entre open hole. Establiced circulation with 450 lpm, 53 bar. Torque readings with 20 rpm, 16-20 kNm, up/down weight, 189/133 ton." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3560m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 7' liner on 5 1/2' DP from 3290 m to 3560 m. Filled every 5th stands. Average running rate 4 stands/hr. Took weight 30 ton. Worked through area from 3561 m to 3551 with 250 lpm, 50 bar, 20 rpm, 19-22 kNm." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4618m. The activity was categorized as 'drilling -- casing' and lasted for 10.5 hours. Operational details: Washed with 7' liner on 5 1/2' DP from 3560 m to 4618 m with 250 lpm, 45 bar. Took weight 10 ton @ 4618 m. Worked string, attempted to pass no success. Worked through area from 3990 m to 4017 with 20 rpm, 23-27 kNm." "On 2013-12-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4677m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Reamed down with 7' liner on 5 1/2' DP from 4618 m to 4677 m with 339 lpm, 61 bar 25 rpm, 23-27 kNm. Took up/down weight 235/120 ton." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4677m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed space out. B/U double and M/U 6m pup joint." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4682m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Reamed down with 7' liner on 5 1/2' DP from 4677 m to 4682 m with 339 lpm, 61 bar 25 rpm, 23-27 kNm. Took up/down weight 235/120 ton." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4682m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: M/U cement head." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Established circulation with 220 lpm, 60 bar and tagged TD with 5 ton. Pulled to up weight 235 ton. Pulled back string 1,5 m to setting depth at 4683 m." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Stepped up circulation to 665 lpm, 89 bar and circulated 1 time open hole volume 18 m3." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Dropped ball and chased with 440 lpm, 65 bar/220 lpm, 45 bar. After 830 stroke ball landed in ball seat. Pressured up to 160 bar for 2 min, Bleed to 100 bar. Set of 30 ton and verified hanger set. Released running tool and sheared ball seat with 220 bar." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Established circulation in steps of 200 lpm to 900 lpm, 10 m3 loss was observed Reduced flow to 700 lpm, 90 bar, no loss observed. Established rotation with 20 rpm, 20-26 kNm. Pressure tested rig up to 345 bar." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: Circulated bottoms up prior to cement job with 800 lpm, 130 bar, 20 rpm, 20-26 kNm." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. Well static." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Pumped 15 m3 of 1,56 SG spacer, 800 lpm, 154 bar. Displaced lines with 1,8 m3 of 1,32 SG OBM, 800 lpm, 130 bar. Closed IBOP and applied 30 bar above. Rotated with 20 rpm, 25-32 kNm." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Mixed and pumped 23,2 m3 of 1,9 SG cement slurry with 600/400 lpm. Displaced cement to rig floor with 890 ltr of drill water. Rotated with 20 rpm, 20-30 kNm." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Displaced the cement with 62 m3 of 1,32 SG OBM with 700 lpm 134 bar. Rotated with 25 rpm, 20-29 kNm. Plug was not bumped. FCP 157 bar with 800 lpm. No losses during cementing and displacing" "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Bleed off pressure and checked for back flow, no flow observed." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: R/D surface lines and sheaves." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4683m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pulled running tool up 3,7 m . Applied 40 ton to set packer. Observed 2 sheares Pulled up and applied 5 ton on packer. Lined up to cement unit and verified line up. Closed annular and tested annulus and packer to 345 bar for 10 min." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3172m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Released hanger running tool. Applied 50 bar on string, pulled up, pressure dropped and increased flow while pulling out of PBR." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3160m. The activity was categorized as 'completion -- other' and lasted for 2.5 hours. Operational details: Circulated out excess cement with 2000 lpm, 120 bar. Diverted 45 m3 of spacer contaminated mud to slops" "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2864m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Broke out cement stand and R/B same in derrick. Installed 2 x sponge ball. Circulated pipe clean with 2000 lpm 105 bar. R/B 2 stands in derrick from 2945 m to 2864 m." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2864m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2864m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 5 m3 of 1,68 SG slug." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2864m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: L/D cement head on deck." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with 5 1/2' landing string/RT from 2864 m to 2505 m . Avg. tripping speed 478 m/hr." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Re-calibrated PRS." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew." "On 2013-12-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: POOH with 5 1/2' landing string/RT from 2505 m to 25 m . Avg. tripping speed 522 m/hr." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed PS-21 from rotary and installed master bushing." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH with liner hanger running tool from 25 m and L/D same on deck." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'completion -- other' and lasted for 2.5 hours. Operational details: P/U and M/U safe lock plug and RIH same to 613 m." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Waited on cement. Performed general rig service." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'interruption -- wait' and lasted for 3.8 hours. Operational details: Waited on cement. Performed preventive maintenance on drill floor equipment." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: De-isolated drill floor equipment and prepared to pressure test well." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Spaces out and closed lower pipe ram with reduced closing pressure. Pulled tool joint up underneath pipe ram and returned to normal working pressure." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Attempted to perform line test to 20/345 bar, no success due to leaking cement unit." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: Cementer repacking around piston. Test unit. Isolated drill floor equipment. Performed PM on ironroughneck and TDS. De-isolated drill floor equipment" "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 613m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Perform line test to 20/345 bar. Attempted to pressure test well to 345 bar, no success. Pumped 2036 ltr received 1500 ltr. Leakage on 138 bar, 1,76 Sg leakoff." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 645m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: RIH with safe lock plug from 613 m to 645 m. Established circulation with 1085 lpm, 25 bar. Washed area from 647 m to 643 m. Took up/down weight prior to set safe lock plug, 97/87 ton." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 645m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Set safe lock plug as per Archer instruction. Element depth 645. Top stinger 642,44 m." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 641m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Spaced out and closed lower pipe ram with reduced closing pressure. Pulled tool joint up underneath pipe ram and returned to normal working pressure." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 641m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Lined up and pressure tested surface lines to 345 bar for 10 min. Pressure tested safe lock plug to 345 barfor 10 min against pipe rams." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 641m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Opened pipe rams. Spotted 5 m3 hi-vis pill 4 m above safe lock plug." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: POOH with safe lock running tool to 160 m." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Cleaned and tidied drill floor. Prepared to displace riser from 160 m to surface." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to displace riser to SW." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Checked line up prior to displace riser to SW. Connected TDS to drill string." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Established circulation with 2400 lpm, 108 bar. Heated up mud for 10 min." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Pumped 10 m3 soap pill and displaced riser to SW with 2400 lpm, 108 bar, 80 rpm, 1-5 kNm." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Closed annular and flushed kill/choke lines with SW. Opened annular." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: POOH with safe lock plug running tool from 160 m and L/D same." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to retrieve wear bushing." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: M/U jet sub assy and wear bushing retrieving tool. RIH to 138 m." "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: M/U TDS and jet wash wear bushing from 138 m to 141 m, 1500 lpm, 67 spm, 10 bar" "On 2013-12-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 166m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH with jet wash assy and wear bushing retrieving tool from 138 m to 166 m." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 185m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH with jet wash assy and wear bushing retrieving tool from 166 m to 185 m." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 172m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: engaged wear bushing and set down 5 ton. Took 33 ton over pull to disengage wear bushing. POOH to 172 m." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 48m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: POOH with wear bushing from 172 m to 48 m. L/U wear bushing and r-tool." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with jet sub assy from 48 m and L/U jet sub assy." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: P/U and M/U PADPRT. RIH with PADPRT to 138 m. Landed sub in WH. Set lock down sub." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Performed line test to 207 bar against HCR. Pressure set lockdown sub. Closed annular and attempted to pressure set no success. Opened annular. Closed upper pipe ram. Pressure set lockdown sub according DOP to 207 bar for 15 min." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Took 30 ton overpull to confirm lockdown sub is set. Reduced weight to 2 ton overpull and released running tool." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with lockdown sub RT and L/D same." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: R/D elevator and rotating arm. Cleaned and cleared rig floor for excess equipment." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to pull diverter." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared to pull diverter. Removed master bushing from rotary. Informed production to shut down production on all wells." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Bleed down koomey unit. Pulled diverter according to procedure. Secured diverter in setback area." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Drained slick joint. Connected slings. Disconnected slick joint from annular. L/D slick joint. Installed master bushing in rotary." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to N/D BOP." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: N/D BOP according to procedure. Disconnected BOP from drilling riser." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Skidded BOP to above BOP test stump. Installed gasket and cleaned inside NT 2 connector. Waited on scaffolders prior to land BOP on test stump." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed BX-elevator and rotating arm." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to M/U Claxton NT-2 running tool." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: P/U Claxton NT-2 running tool. Removed master bushing and drive ring. Ran Claxton NT-2 running tool through rotary. Installed master bushing and drive ring. M/U and ran Claxton NT-2 running tool to 1 m above BOP drilling riser joint." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Set dogs and landed Claxton NT-2 running tool on BOP drilling riser joint." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: M/U Claxton NT-2 running tool to BOP drilling riser joint according to procedure. Performed pre-job meeting with crew prior to disconnect riser tensioner system." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled up 135 ton on string to take weight off riser tensioner system. TDS, weight indicator 152 ton." "On 2013-12-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Reduced hydraulic pressure on riser tensioner system in steps and transfer all load to top drive. Started to disconnect cylinders from tension ring according to procedure. Simultaneously prepared Well Partners equipment on drill floor. Removed scaffold from riser in moonpool." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Disconnected cylinders from tension ring according to procedure." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Prepared 10 ton moonpool winch for use as guidewire. Built scaffold around slot F-10 prior to remove hatches for guidewire access." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed hatches on well head and moonpool area. Meanwhile landed BOP onto test stump." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Assisted ROV to install 10 ton guidewires to tempplade and riser clamp. Built scaffold around moonpool hatch opening." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran 6 ton guidewire, connected to tempplade and riser clamp. Applied tension on 10/6 ton guidewire. Informed production to shut down F-14 and F-9 at 05:15 hrs." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared and R/U to run hot stab." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Connected hot stab to guidewire. Started to run hot stab in sea." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed dummy hot stab, flushed hot stab and installed hot stab. ROV functioned TBC panel to primary unlock." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Slacked off on TCB Weight indicator reading 103 ton. Pressured up hot stab to 3000 psi. P/U 20 cm. ROV reset TBC valves according procedure. Removed hot stab and installed dummy." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up on HPDR. Weight indicator reading 120 ton." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to R/U and POOH HPDR." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Retrieved hot stab to surface." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Pulled up HPDR 4 m. ROV inspected well head no seal ring observed." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed master bushings and outer ring. Install HPDR spider and control lines, function test same." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 129m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled up HPRR BOP joint. Inserted c-plate, installed 24' elevators and landed off joint." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 129m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: B/U BOP joint, installed protector on flange and L/D same on cantilever." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 129m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed auto elevators and rotating arm." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 59m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 7.2 hours. Operational details: POOH with HPDR joints from 129 m to 59 m. Attached protectors and L/D joints on cantilever. Removed 24' sidedoor elevators and installed auto elevator. Informed production to shut down all production at 18:20 hrs." "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 59m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with new crew" "On 2013-12-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: POOH with HPDR joints from 59 m to 21 m. Attached protectors and L/D joints on cantilever. Disconnected guidewire from template with assistance of ROV. Retrieved guidewires. Installed guide funnel." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: POOH with HPDR joints from 21 m. Attached protectors and L/D joints on cantilever." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed lifting sub from Stress Joint /TBC and installed protector. L/O Stress Joint / TBC." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared rig floor for HPDR fairings. P/U and landed HPPR fairings on rig floor and secured same." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed bolt protection to production TBC and installed lifting subs to HPPR, first 3 joints." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to P/U and run production riser." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up tieback connector and stress joint, landed same in riser spider. Picked up lower riser pup joint from cantilever." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crews." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 11m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Inspected seal faces and installed IX-14 ring gasket. Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser through rotary and spaced out to test tieback connector." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 11m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Function tested tieback connector." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 37m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Picked up standard riser joint #1 and made up to riser pup joint. Inspected seal faces and installed IX-14 ring gasket. Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser and landed same in riser spider." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 52m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up standard riser joint #2 and made up to standard riser joint #1. Inspected seal faces and installed IX-14 ring gasket. Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser and landed same in riser spider." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 66m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Picked up standard riser joint #3 and made up to standard riser joint #2. Inspected seal faces and installed IX-14 ring gasket. Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser and landed same in riser spider." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 81m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Picked up standard riser joint #4 and made up to standard riser joint #3. Inspected seal faces and installed IX-14 ring gasket. Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser and landed same in riser spider." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 95m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Picked up splash zone riser joint and made up to standard riser joint #4. Inspected seal faces and installed IX-14 ring gasket. Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser and landed same in riser spider." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 102m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Picked up upper riser pup joint and made up to splash zone riser joint. Inspected seal faces and installed IX-14 ring gasket. Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser and landed same in riser spider." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 102m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to pick up tension joint." "On 2013-12-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 102m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up tension joint and made up to upper riser pup joint. Inspected seal faces and installed IX-14 ring gasket." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 102m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up bolted flange connection. Pressure tested flange connection to 207 bar through test port, ok. Installed fairings. Lowered riser and landed same in riser spider. Installed hang off clamp." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up and made up pre-made 5 1/2' DP landing string to tension joint." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to rigging down riser spider." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed hang off clamp." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged down riser spider and installed master bushings." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to landing riser / tieback connector." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lowered riser to approx. 0,2 meter above guide funnel. Adjusted guide line wires. Stabbed tieback connector into riser guide funnel on WH." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed guide funnel. At 04:45 hrs. informed Production to resume according to SIMOPS." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Lowered hot stab on guide wire. Observed guide wire tangled around well F-5. Disconnected guide wire on template and untangled same. Connected hot stab to TBC using ROV. Meanwhile cleared and cleaned rigfloor." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Landed off tieback connector on well head with 15 Ton. Locked connector according to procedure, observed stroke indicator indicating TBC fully locked." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Filled production riser and pressure tested same to 20 / 200 bar 5 / 10 minutes. Pumped 540 liter. Bled back 505 liter." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Flushed tieback connector control lines. Sat all valves in lock position. Recovered hot stab to surface." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Recovered guide line wires to surface." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to installation of moonpool hatches." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed F-15 hatches." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to installation of tensioner system." "On 2013-12-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: Installed riser centralizers, tension ring and tension cylinders. Meanwhile pressure tested BOP on stump to 20 / 345 bar - 5 / 10 minutes." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Installed riser centralizers, tension ring and tension cylinders. Meanwhile pressure tested BOP on stump to 20 / 345 bar - 5 / 10 minutes." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to cut and bevel riser." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Rigged up production riser cutting tool." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Cut production riser. At 07:15 hrs informed production to shut down prior to recovering cut off piece." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Waited on production to shut down. Meanwhile prepared to run Multibowl WH." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled cut off riser piece to drill floor and laid out same. Commenced bevelling of production riser." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Bevelled production riser edge. Meanwhile picked up and prepared BOP riser joint." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Made up BOP riser joint to Multibowl in well center." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up BOP joint and Multibowl. Removed master bushings and split hatch cover. Ran multibowl and BOP joint through rotarty on chain slings. Landed out Multibowl onto surface riser." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Tested Multibowl BT and FS seals. Energized plastic in upper and lower BT seals and tested same. Meanwhile tested BOP to 20 / 345 bar - 5 / 10 minutes." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Energized Multibowl slips. Performed 5 Ton overpull test, ok." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed moonpool hatches around production riser." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Installed Multibowl annulus valves and tested same to 30 / 345 bar - 5 / 10 minutes. Meanwhile: Erected scaffolding around BOP riser joint. Removed chains from BOP riser joint and pulled same to rigfloor. Prepared for nippling up BOP." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to nipple BOP." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Moved BOP to well center and landed same onto riser. Made up NT2 connector. Picked up and ran slick joint, made up same to BOP. Installed diverter. Connected tension system and energized same. At 22:30 informed production to resume according to SIMOPS." "On 2013-12-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to running bowl protector" "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up bowl protector running tool and made up to 5 1/2' DP. RIH and installed bowl protector in Multibowl WH. POOH and broke out bowl protector RT." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up and made up jetsub to 5 1/2' DP. RIH with jetsub assembly to 150 meter. Pumped 14 m3 hi-visc pill and chased same with SW at 1800 liter/min, 7 bar. Picked up slowly from 150 m to 130 m while circulating SW at 1330 liter/min, 5,5 bar. POOH with Jetsub assembly and laid out same." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Picked up and RIH with annulus insert retrieval tool from surface to 139,81 meter. Pulled annulus insert free. Displaced riser to brine at 1800 liter/min, 2,5 bar. POOH with annulus insert retrieval tool and insert, laid down same." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleared and cleaned rigfloor." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crews." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: RIH with bowl protector retrieval tool and attempted to retrieve bowl protector from Multibowl WH. POOH with retrieval tool, bowl protector not engaged to retrieval tool. RIH with bowl protector retrieval tool and retrieved bowl protector from Multibowl WH at 20,87 meter." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rig up handling equipment." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 9.5 hours. Operational details: Rigged up handling equipment for 10 3/4' tie-back casing. Picked up and made up DQ adjustable tool." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to run 10 3/4' tie-back casing." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 10 3/4 tie-back adapter and inspected same." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crews prior to run 10 3/4' tie-back casing." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up and RIH with 10 3/4' tie-back string from surface to 107,5 meter." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 108m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.8 hours. Operational details: Not able to pick up 10 3/4' hanger from main deck due to wind speeds above crane operational limitations. Held toolbox talk prior to pick up hanger." "On 2013-12-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 10 3/4' surface hanger with adjustment sub." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 10 3/4' tie-back casing and landed same with 2 Ton. Engaged tie-back connector by rotating 6 RH turns using elevator. Land off point at 139,8 meter." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out 10 3/4' casing landing string and laid down same onto HTS." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rigging down casing handling equipment." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Changed to 5 1/2' DP handling equipment." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and made up tie-back torque tool." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with tie-back adapter torque tool. Made up TDS and torqued up tie-back adapter to 1300 Nm." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with tie-back adapter torque tool and laid out same." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged up 10 3/4' casing handling equipment for tie-back casing." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and RIH with 10 3/4' casing landing string. Not able to screw into RT threads." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: POOH with 10 3/4' casing landing string. Checked threads, filed same. RIH with 10 3/4' casing landing string and engaged same." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made up swedge to landing string. Performed overpull test to 170 Ton." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Rigged up surface hose and swedge, tested same to 345 bar - 5 minutes. Pressure tested surface tie-back casing against safe lock plug to 30 / 345 bar - 5 / 10 minutes. Rigged down surface lines and swedge." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up adjustable sub setting tool on 5 1/2' DP and RIH to 29 m. Not able to locate torque slots in adjustable sub. POOH with adjustable sub setting tool on 5 1/2' DP and inspected same. RIH with tool to 29 m. Engaged adjustable sub setting tool." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Applied 130 bar to adjustable sub setting tool, picked up to 2 Ton overpull and bled off pressure. Rotated string 14,5 turns clockwise. Took 22 Ton overpull and pressured up to 130 bar. Bled off pressure, rotated clockwise untill reading 11000 Nm, weight dropped off. Waited 3 minutes and retrieved adjustable sub setting tool to surface." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged up surface hose and swedge, tested same to 345 bar - 5 minutes. Pressure tested adjustable sub internal seal against safe lock plug to 30 / 345 bar - 5 / 10 minutes. Rigged down surface lines and swedge." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Disengaged casing hanger running tool. POOH and laid down 10 3/4' landing string. Rigged down 10 3/4' casing handling equipment." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to run MS-T seal assembly." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Picked up 10 3/4' MS-T seal assembly RT and made up same to 5 1/2' DP. Installed MS-T seal on RT. RIH with seal assembly on 5 1/2' DP, landed off at 20,50 meter. Locked seal assembly into riser, confirmed lock with 4 Ton overpull. Set MS-T seal assembly." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Tested MS-T seal assembly to 345 bar - 10 minutes through multi bowl port. POOH with 10 3/4' MS-T seal assembly RT and laid down same." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Held toolbox talk prior to test. Closed shear rams and lined up to test. Pressure tested BOP connection against safe lock plug to 20 / 345 bar - 5 /10 minutes. Opened shear rams." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Performed pre-job meeting. Picked up bowl protector RT and made up to 5 1/2' DP. RIH and installed bowl protector in Multibowl WH." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH and laid down bowl protector RT." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to retrieval of Safe lock plug." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 170m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Picked up Safe Lock plug RT and made up to 5 1/2' DP. RIH with Safe Lock plug RT on 5 1/2' DP from surface to 170 m with restricted speed." "On 2013-12-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 170m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to displacement." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 170m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Displaced riser from 1,03 sg packer fluid to 1,32 sg OBM." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 637m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: RIH with Safe Lock plug RT on 5 1/2' DP from 170 m to 637 m." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 640m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: At 637 meter made up TDS and commenced circulation with 200 liter/min, 15 bar. Pulled back to 627 meter. Increased flow rate to 2500 liter/min, 46 bar and displaced hi-visc pill out of well. Decreased rate to 250 liter/min, 10 bar and washed back down to 640,4 meter. Increased flow rate to 2500 liter/min, 47 bar for three minutes to remove any debris from plug." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 640m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Continued to wash down with 150 liter/min to top of plug at 642,4 m. Latched onto plug. Set down 10 Ton on plug, rotated string 3/4 RH turn, took 15 Ton overpull. Slacked off 2 Ton weight and applied 35 bar, observed pressure drop to 4,8 bar. Took 2 ton overpull and rotated 30 clockwise turns to release plug. RIH past plug setting depth to verify plug retrieved and free, ok" "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 640m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Circulated bottom up with 1000 liter/min, 26 bar." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.5 hours. Operational details: Performed flow check for 10 minutes, ok. POOH with Safe Lock plug on 5 1/2' DP from 640 m to surface with restricted speed. Inspected Safe Lock Plug and laid out same." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.0 hours. Operational details: Cleared rigfloor from excess equipment. Laid out 10 3/4' casing handling equipment and various WH tools. Picked up Running tools and plugs for operations." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Rigged up 3 1/2' DP handling equipment." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to make up BHA." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 105m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.2 hours. Operational details: Picked up mill assembly and broke off mill, made up 6' bit with bitsub and float. RIH from surface to 105 meter." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 940m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 8.2 hours. Operational details: Picked up 3 1/2' DP singles while RIH with 6' clean out BHA from 105 m to 940 m. Average tripping speed 98 meter/hour." "On 2013-12-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 940m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Filled pipe at 940 meter." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1504m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 6.0 hours. Operational details: Picked up 3 1/2' DP singles while RIH with 6' clean out BHA from 940 m to 1504 m. Average tripping speed 93 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1504m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed from 3 1/2' to 5 1/2' DP handling equipment." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1994m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 1504 m to 1994 m. Average tripping speed 488 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1994m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied trip tank. Made up TDS and filled pipe." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 1994 m to 2317 m. Average tripping speed 646 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied trip tank." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2721m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 2317 m to 2721 m. Average tripping speed 700 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2721m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied trip tank." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3000m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 2721 m to 3000 m. Average tripping speed 710 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3000m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied trip tank." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3325m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 3000 m to 3325 m. Average tripping speed 650 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3325m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied trip tank." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3649m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 3325 m to 3649 m. Average tripping speed 648 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3649m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied trip tank." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4010m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 3649 m to 4010 m. Average tripping speed 722 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4010m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Emptied trip tank. Problems with empty trip tank due to thick mud. Made up TDS and filled pipe, broke circulation with 550 liter/min, 75 bar, circulated 15 minutes." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4600m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH with 6' clean out BHA on 5 1/2' DP from 4010 m to 4600 m. Average tripping speed 786 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4630m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Made up TDS and established circulation. Washed and scraped from 4600 m to 4626 m with 500-950 liter/min, 95-205 bar, made three passes of interval. Circulated 1 x bottoms up with 885 liter/min, 209 bar. Reciprocated pipe between 4625 m and 4600 m. RIH with 6' clean out assembly and tagged landing collar at 4630 m, sat down 4 Ton. No cement observed in returns." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4602m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: POOH with 6' clean out BHA on 5 1/2' DP from 4630 m to 4602 m." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4602m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flow checked well for 15 minutes, static." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4602m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up TDS and pumped 4 m3 1,62 sg slug, chased same with 4,5 m3 1,32 sg OBM." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3772m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: POOH with 6' clean out BHA on 5 1/2' DP from 4602 m to 3772 m. Restricted tripping speed to 1 minute / stand." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3772m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Filled trip tank." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3531m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: POOH with 6' clean out BHA on 5 1/2' DP from 3772 m to 3531 m. Restricted tripping speed to 1 minute / stand." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3531m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2276m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: POOH with 6' clean out BHA on 5 1/2' DP from 3531 m to 2276 m. Restricted tripping speed to 1 minute / stand until past 3100 meter" "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2276m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Filled trip tank." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: POOH with 6' clean out BHA on 5 1/2' DP from 2276 m to 1634 m. Average tripping speed 890 meter/hour." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held pre-job meeting." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Changed from 5 1/2' to 3 1/2' DP handling equipment. Commenced POOH with 6' clean out assembly on 3 1/2'. While racking first 3 1/2' DP stand, the stand slipped out of the PRS claw and leaned against the derrick." "On 2013-12-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1634m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Recovered stand back into PRS." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1634m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Recovered stand back into PRS. Inspected PRS, replaced broken split pin in claw." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Installed PS-21 power slips." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1120m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: POOH with 6' clean out BHA on 3 1/2' DP from 1634 m to 1120 m. Average tripping speed 295 meter/hour. Observed stuck finger in 3 1/2' DP fingerboard." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1120m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired stuck finger in 3 1/2' DP fingerboard." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 392m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: POOH with 6' clean out BHA on 3 1/2' DP from 1120 m to 392 m. Average tripping speed 364 meter/hour." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 392m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TBT with day shift for POOH on 3 1/2' DP." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 105m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: POOH w/ 6' clean out BHA on 3 1/2' DP from 392 m to 105 m. Avg. tripping speed 164 m/hr. Controlled tripping speed to ensure stands correctly latched in fingerboard." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 105m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TBT for L/O 6' BHA." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: POOH and L/D 6' clean out BHA." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing well." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Attempted to pressure test well to 253 bar w/ 1,32 sg OBM. Observed pressure drop from 243 bar to 160 bar. Bled down pressure." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed TBT for M/U Interwell ME plug assy." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: P/U and M/U the 7' ME plug as per Interwell instructions using the foxhole. M/U 3 1/2' DP stand to plug RT." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 235m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: RIH w/ ME plug on 3 1/2' DP from surface to 235 m. Avg. tripping speed 235 m/hr." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 235m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Emptied T/T." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 465m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: RIH on 3 1/2' DP from 235 m to 465 m. Avg. tripping speed 306 m/hr." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 465m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Changed from PS21 to Odfjell slips." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 494m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: RIH on 3 1/2' DP from 465 m to 494 m." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 494m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Broke circulation w/ 225 l/min, 22 bar." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1012m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: RIH w/ ME plug on 3 1/2' DP from 494 m to 1012 m. Avg. tripping speed 296 m/hr." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1012m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Broke circulation w/ 200 l/min, 25 bar." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1529m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: RIH w/ ME plug on 3 1/2' DP from 1012 m to 1529 m. Avg. tripping speed 345 m/hr." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1529m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Changed to 5 1/2' handling equipment. Broke circulation." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2012m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: RIH w/ ME plug on 5 1/2' DP from 1529 m to 2012 m. Avg. tripping speed 483 m/hr." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2012m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Broke circulation w/ 200 l/min, 28 bar." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2421m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: RIH 5 1/2' DP from 2012 m to 2421 m. Avg. tripping speed 545 m/hr." "On 2013-12-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2421m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Stopped RIH due to wind speed above limit for PRS (> 65 kts). WOW." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2421m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: WOW, wind speed above PRS limit (> 65 kts). Monitored well on T/T. Broke circulation w/ 120 l/min, 28 bar." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2821m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: RIH w/ 7' ME plug on 5 1/2' DP from 2421 m to 2821 m." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2821m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Experienced problems with aft iron roughneck. Isolated IRN and investigated failure. Meanwhile broke circulation w/ 120 l/min, 28 bar." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2821m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Repaired aft IRN. Meanwhile monitored well on T/T." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3345m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: RIH w/ ME plug on 5 1/2' DP from 2821 m to 3345 m. Avg. tripping speed 524 m/hr." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3345m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Broke circulation w/ 150 l/min, 28 bar." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3872m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 3345 m to 3872 m. Avg. tripping speed 527 m/hr." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3872m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Broke circulation w/ 150 l/min, 29 bar." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4315m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: RIH on 5 1/2' DP from 3872 m to 4315 m. Avg. tripping speed 590 m/hr." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4315m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Broke circulation w/ 120 l/min, 30 bar." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4598m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: RIH on 5 1/2' DP from 4315 m to 4598 m. Avg. tripping speed 377 m/hr." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4598m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Dropped ball and M/U TDS to last stand." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4621m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: RIH to 4625 m, pulled up to setting depth 4621 m with plug seals at 4620 m. Pumped ball with 170 l/min, 40 bar and set plug as per Interwell instructions. Load tested the plug with 5 T down weight." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4621m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4621m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Lined up and pressure tested the surface lines. Pressure tested the 7' ME plug against upper pipe ram to 253 bar/ 10 min. Pumped 1832 l, bled back 1772 l." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4621m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Flowchecked, well stable." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4598m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Pulled stand wet. Pumped slug and chased same." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4072m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: POOH on 5 1/2' DP from 4598 m to 4072 m. Avg. tripping speed 420 m/hr." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4072m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Pumped slug and chased same." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1529m. The activity was categorized as 'completion -- other' and lasted for 3.0 hours. Operational details: POOH w/ ME plug RT on 5 1/2' DP from 4072 m to 1529 m. Avg. tripping speed 848 m/hr." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1529m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Changed to 3 1/2' handling equipment." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1529m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling and racking 3 1/2' DP stands." "On 2013-12-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 850m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: POOH w/ ME plug RT on 3 1/2' DP from 1529 m to 850 m. Avg. tripping speed 453 m/hr." "On 2013-12-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.2 hours. Operational details: POOH w/ ME plug RT on 3 1/2' DP from 850 m to surface. Avg. tripping speed 378 m/hr." "On 2013-12-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Broke 3 1/2' DP stand and RT in foxhole. L/D plug RT." "On 2013-12-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Changed handling equipment to 5 1/2'. Cleaned and cleared rig floor. *** Note *** Further operations for suspending F-15 D will be reported on F-1B - well intervention." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Installed walkways and stair after skidding cantilever from F-1 to F-15 slot. ******NOTE: From 00:00-08:30 reported on F-1 B******" "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 4.0 hours. Operational details: Cleared rig floor of AWS and SLB equipment from F-1 B well intervention, packed same for backload." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.5 hours. Operational details: Performed TBT. Rigged up, slipped and cut drill line. Cleaned and cleared rig floor. Performed brake calibration test. Meanwhile backloaded W/L equipment." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Errected scaffold access stairwell and handrails in moonpool. Meanwhile installed shackles and chains on bails. P/U BOP riser and landed same in set back. Prepared hatches on F-15 slot. Backloaded cargo. Re-installed flowline covers." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT prior to changing hatches on wellhead module." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Removed bolts from full hatch, lifted hatch from slot F-15. Installed split hatches and M/U same. Informed production department at 20:00 hrs to shut in wells as per SIMPOPS procedure." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Waited on production department to confirm wells depressurized. Meanwhile prepared for installation of BOP riser and arranged equipment on pipe deck." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Received note from production department. Lowered BOP riser joint to mulitbowl. M/U riser joint." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Fit split covers on hatch. Performed TBT for building scaffold around BOP riser joint." "On 2013-12-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Built scaffold around riser to M/U NT2 connector." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Built access scaffold around BOP riser joint in moonpool." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lifted BOP from stump. Skidded BOP to well centre." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Held TBT and skidded cantilever to allign BOP with well center." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Landed BOP on riser." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lowered and landed slick joint on BOP. M/U same. Informed production department at 04:20 hrs. to re-start production as per SIMOPS procedure." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: M/U NT2 connector" "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: M/U slick joint and installed BOP tensioners. Meanwhile picked up diverter." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT with day shift." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Installed remaining tensioners." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Alligned BOP and installed diverter." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Filled riser and BOP with SW." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pressure tested riser and BOP connector against Safelock plug to 20/345 bar 5/10 min." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: R/D and layed out diverter chains and bridle. Cleared rig floor." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: P/U and M/U Archer Safelock plug retrieval tool." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Installed PS21 slips." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 610m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: RIH w/ Safelock RT on 5 1/2' DP from surface to 610 m. Avg. tripping speed 349 m/hr." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 628m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Washed in from 610 m to 628 m w/ 200 l/min, 9 bar. At 628 m circulated out HiVis pill with 2400 l/min and 48 bar." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 631m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Engaged plug as per Archer instructions. Used several attempts with 10 -20 t set down weight. Confirmed latch with 10 t overpull." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 631m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Opened ball valve and observed pressure drop. Released plug and allowed element to retract. RIH to 635 m to confirm plug free." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 630m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Flowchecked, well stable." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 40m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: POOH w/ Safelock plug on 5 1/2' DP from 630 m to 40 m. Reduced speed while tripping due to winds close to PRS operating limit." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 40m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed master bushing." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: POOH and L/D the 9 5/8' Safelock plug and RT. Inspected same, no damage." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: R/U 3 1/2' handling equipment for clean-out BHA." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TBT." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: M/U 6' cement mill to clean-up assembly #1 (scraper and magnets for 7' liner)." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 215m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH w/ clean-out assy #1 on 3 1/2' DP from surface to 215 m. Reduced running speed due to high wind." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 215m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21 slips." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: RIH on 3 1/2' DP from 215 m to 1430 m. Avg. tripping speed 486 m/hr. Reduced running speed due to high wind." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Installed rotator on bails." "On 2013-12-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to P/U clean-out assembly #2 (tieback mill, well commissioner, magnets). Wind speed above crane limit. Meanwhile cleaned in drilling areas, performed high wind checks and housekeeping." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather to P/U clean-out assembly #2. Wind speed above crane limit. Meanwhile cleaned in drilling areas, performed high wind checks and housekeeping." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: P/U and M/U clean-out assembly #2 (Well commissioner)." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TBT with day shift for picking up BHA." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Lifted assy #2 with PDM. P/U and M/U same." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW to pick up assy #4, wind speed above crane limit." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1463m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: P/U and M/U assembly #4 and RIH to 1463 m." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1463m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation at 1463 m w/ 600 l/min, 72 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1990m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH w/ clean-out BHA on 5 1/2' DP from 1463 m to 1990 m. Restricted speed to 1 min/stand." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1990m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation at 1990 m w/ 600 l/min, 55 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2500m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 1990 m to 2500 m. Restricted speed to 1 min/stand." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2500m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation at 2500 m w/ 600 l/min, 56 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2960m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 2500 m to 2960 m. Restricted speed to 1 min/stand." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2960m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation at 2960 m w/ 600 l/min, 56 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3158m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH on 5 1/2' DP from 2960 m to 3158 m. Restricted speed to 1 min/stand." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3158m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation at 3158 m w/ 500 l/min, 37 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3197m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Washed in from 3158 m to 3197 m w/ 500 l/min, 36 bar, 20 RPM, 13 kNm." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3562m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 3197 m to 3562 m." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3562m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation at 3562 m w/ 600 l/min, 51 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4086m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 3562 m to 4086 m." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4086m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation at 4086 m w/ 600 l/min, 72 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4098m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: P/U and M/U clean-up assembly #5. RIH to 4098 m." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4560m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 4098 m to 4560 m." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4560m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Scraped packer area. Reciprocated string +/- 15 m in packer area, 40 RPM / 16 kNm and pumping w/ 600 l/min/ 108 bar." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4607m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: M/U last stand. Entered PBR with polish mill, tagged w/ 3 t at 4607,4 m. Pollished PBR as per program." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4607m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated the 7' liner w/ 1000 l/min, 267 - 204 bar, 60 rpm. Reciprocated string. Circulated 4x liner volume. While circulating, performed TBT for pumping base oil and inflow testing the 7' liner." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4607m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Landed string on PBR, sheared MFCTC tool w/ 17 t as per Swaco SPS instructions. Verified tool in open position." "On 2013-12-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4607m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Established circulation. Circulated and conditioned mud w/ 3500 l/min, 278 - 250 bar. Rotated string with 90 rpm, 11-15 kNm." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated and conditioned mud w/ 3500 l/min, 278 - 250 bar. Rotated string with 90 rpm, 11-15 kNm. Circulated until even MW in/out." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Picked up and cycled MFCTC tool into closed position." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Set the well commissioner. Lined up to pump down kill line. Closed BOP and pressure tested packer element with 70 bar. Unset well commissioner. Set MFCTC tool into closed position and verified same." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Flushed standpipe. Displaced string to base oil, 500 l/min, FCP 127 bar. Static pressure: 93 bar. Pumped 28,2 m3." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Monitored pressure and well on trip tank. Confirmed well stable with drillpipe pressure 92 bar." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Equalized pressure with the cement unit. Inflow tested well. Bled down in steps of 30 bar to 5 bar. Monitored pressure. Good test, 0,8 bar/ 30 min increase. Increased DP pressure back to 93 bar." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Unset well commisioner and allowed element to relax. Isolated cement unit and bled back on cement line." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Flushed remaining surface lines and c/k manifold. Cleaned slips and bell nipple." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TBT prior to displacing well to completion brine." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Prepared pits for displacement, transfered OBM into holding tanks." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pumped wash train and 67 m3 of completion brine (7' liner volume + 200 m excess), 1800 - 1900 l/min, 246 - 260 bar." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4607m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Set down string w/ 15 t on PBR, opened MFCTC tool. Confirmed tool open w/ 500 l/min." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4607m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Displaced the well above TOL to completion brine with 4000 l/min, 165 - 144 bar, 60 rpm, 11-22 Nm." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4607m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Cycled MFCTC tool to closed position, allowed element to relax." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Closed BOP (MPR), lined up and pressure tested well to 345 bar/ 10 min. Pumped 2350 ltr, bled back same volume." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4606m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flowchecked well for 30 min, well stable." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3172m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: POOH w/ clean-up BHA on 5 1/2' DP from 4606 m to 3172 m. Avg. tripping speed 521 m/hr. Restricted speed to 1,5 min/stand until assembly out of 7' liner." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1472m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: POOH on 5 1/2' DP from 3172 m to 1472 m. Avg. tripping speed 850 m/hr." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1472m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed auto slips and installed master bushing." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1439m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: L/D clean-up assemblies #3 (Wellpatroler and MFCTC) and #4 (magnets)." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1439m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed to 3 1/2' handling equipment." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: L/D clean-up assembly #2 (Wellcommissioner, drift, magnets, polish mill)." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Installed roller assembly on HTS." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1546m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: RIH 4 stands 3 1/2' DP from derrick from 1430 m to 1546 m." "On 2013-12-29, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1001m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: L/D singles while POOH w/ clean-up assembly #1 on 3 1/2' DP from 1546 m to 1001 m. Avg. tripping speed 182 m/hr, 19 singles/hr." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 15m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.0 hours. Operational details: L/D singles while POOH w/ clean-up BHA on 3 1/2' DP from 1001 m to 15 m. Avg. tripping speed 247 m/hr. 26 singles/hr." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: L/D 7' liner clean-up assembly (cement mill, scraper, magnets)." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed handling equipment to 5 1/2'." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: M/U bowl protector retrieval tool." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH to 20,5 m, engaged bowl protector in multibowl surface WH. POOH and L/O bowl protector." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 25m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U jetting sub, RIH to 25 m. Jetted multibowl and tubing hanger setting area. POOH and L/D jet sub." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 10.2 hours. Operational details: WOW to R/U for running completion. Wind speed above crane limit. Meanwhile performed maintenance on PRS, TDS and blocks. Serviced drilling and rig floor equipment. Performed fluid end inspection on MP 2. BOT tested control line reel on main deck. Performed cleaning and housekeeping." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 3.5 hours. Operational details: Bundled 3 1/2' DP and cleared port aft bay. Commenced laying out 7' tubing." "On 2013-12-30, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 4.0 hours. Operational details: Prepared for running completion. Layed out 7' tubing and lifted tubing running equipment to drillfloor. R/U to run 7' completion, lifted SLB reel and equipment to rig floor." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: WOW to lay out 7' tubing. Wind speed above crane limit (50 - 60 kts). Meanwhile R/U SLB reel on rigfloor." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 3.5 hours. Operational details: R/U for running completion and layed out 7' tubing. R/U Baker reel on rig floor, installed Weatherford slips." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 10.0 hours. Operational details: R/U for running completion and layed out 7' tubing. SLB prepared equipment on rig floor. Installed and function tested Weatherford power tong and slips. Worked supply vessel in weather window and P/U remaining lifts, offloaded brine and backloaded slops. Released vessel." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT prior to run completion." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Experienced platform shut-down. Restarted power supply for drilling systems." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: WOW to P/U completion assembly #1 (SAM and perforated pup). Wind speed above crane limit." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Lifted completion assembly #1 on HTS. Attempted to P/U assembly. Experienced malfunction of Weatherford elevator open/close function. Troubleshot w/o success. Changed out to Maersk elevator." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 19m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: P/U and RIH completion assembly #1. M/U 7' tubing with installed EVO plug (assembly #2) to same and RIH to 18,8 m." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 37m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: P/U and M/U 7' tubing joint and completion assembly #3 (Baker packer). RIH to 37 m." "On 2013-12-31, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 107m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 37 m to 107 m. Average 6 joints/hr." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 237m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: RIH with 7' 29# ppf 13%CrS-110 VamTop tubing from 107 m to 237 m. Average 5,5 joints/hr." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: P/U and M/U Schlumberger DHPG assembly. Terminated cable and pressure tested gauge." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 296m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 250 to 296 m. M/U cable clamp on every connection." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1198m. The activity was categorized as 'completion -- completion string' and lasted for 13.0 hours. Operational details: Continued RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 296 to 1198 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals. Average 5,9 joints/hr." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1235m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Continued RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 1198 to 1235 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1235m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Changed jaws on casing tong and L/D joint #175." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1316m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Continued RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 1235 to 1316 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1316m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Changed jaws on casing tong and L/D joint #167 and 168." "On 2014-01-01, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1445m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Continued RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 1316 to 1445 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals. Average speed: 5,3 joints/hr" "On 2014-01-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1892m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: Continued RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 1445 to 1892 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals. Average speed: 6,3 joints/hr" "On 2014-01-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2669m. The activity was categorized as 'completion -- completion string' and lasted for 7.8 hours. Operational details: Continued RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 1892 to 2669 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals. Average speed: 8,5 joints/hr" "On 2014-01-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2676m. The activity was categorized as 'completion -- completion string' and lasted for 3.2 hours. Operational details: P/U and M/U DHSV and installed one joint above. Installed hang off sheave and connected control lines. Tested same to 690 bar." "On 2014-01-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2829m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 2676 to 2829 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals." "On 2014-01-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2829m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed Toolbox talk with ongoing crew." "On 2014-01-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'completion -- completion string' and lasted for 4.5 hours. Operational details: RIH with 7' 29 ppf 13%CrS-110 VamTop tubing from 2829 to 3146 m. M/U cable clamp on every connection. Difficulties to install clamps due to squared cable and changing dies on power tong on regular intervals. Average speed: 6 joints/hr" "On 2014-01-02, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held Toolbox Talk." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Continued to remove power rollers and HTS. Changed handling equipment. Removed control line sheaves to allow PRS to take 5 1/2' DP stand from fingerboard." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3150m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Made up 7' swedge to DP landing stand in foxhole. M/U landing stand with swedge to tubing string. Connected TDS. Rigged up control line sheaves. Removed Autoslips and installed Master bushing. installed control line clamp." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3170m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: RIH on 5 1/2' Dp landing string and entered PBR with Muleshoe. Sheared out but took 5 T weight. Pulled up and RIH to enter PBR second time. Took 7 T weight. Pulled up and experienced 6 T overpull." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3170m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Evaluated situation." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3175m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Started circulation with 150 LPM/5 bar. Pulled Muleshoe free with 17 T overpull. Dropped down to neutral weight. Increased flow to 200 LPM/5 bar. Pulled up 6 m. RIH and enterede PBR again without restriction seen. Btm seen at 3175 m. Measured pipe and calculated spaceout. Pulled out of PBR without restictions. Stopped pump." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Pulled DP stand and removed swedge." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Backed out TDS and stand from 7' tubing string." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3146m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Changed handling equipment." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3148m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: P/U 7' pup joint E" "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3151m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: P/U 7' pup joint C. Changed tong jaws and remade connection." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3151m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Pulled back and installed control line clamp." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3151m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U tubing hanger and fitted clamps to pup joints." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3151m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Stripped back control lines and tested all lines and connections to 35/450 bar for 5/10 min." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3151m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U THRT" "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3151m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Connected lines and tested DHSV to 520 bar for 10 min. Connected THRT lock/unlock lines." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up llanding pup joint and joint. Landed out TH." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Verified correct land out and function tested lock down ring." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Took 15 T overpull test." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested Hanger seals on multi bowl to 35/345 bar for 5/10 min." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Dropped ball and M/U circulation swedge and rig hoses." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Circulated down ball with 150 LPM to seat in EVO plug." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressured up tubing to 70 bar for 5 min. Function tested DHSV and confirmed valve closed and non leaking. Opened DHSV." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pressured up tubing to 345 bar for 30 min for setting Production Packer and testing tubing." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Bled back pressure from 345 bar to 280 bar by bleeding off 70 ltr. Closed DHSV and bled off pressure above to 210 bar by bleeding off 35 ltr. Performed 70 bars diff pressure inflow test on DHSV for 30 min. Bled off to 10 bar above DHSV by bleeding off 105 ltr. Performed 270 bar diff pressure inflow test of DHSV for 10 min. Equalized and opened DHSV. Bled off pressure to zero bar." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lined up to test down A-ann and performed line test to 35/345 bar for 5/10 min." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Leak tested Production Packer from above by applying 35/345 bar for 5/30 min down a-ann. Volumes pumped: 300 / 1030 ltr. Bled off pressure to zero by bleeding off 1130 ltr." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Rigged down pressure testing hose. B/O 7' swedge and L/D same." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Prepared for R/U wireline equipment. Simultaneously bled off control line pressure on DHSV." "On 2014-01-03, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Held Tool Box talk for picking up WL tools." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: R/U wireline equipment. Started to P/U GS toolstring. Problem with winch brake band occured." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Trouble shooted WL winch brake band problem." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Continued to M/U GS toolstring." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Opened DHSV and RIH with GS tool on WL to 264 m. Problems with spooling arm occured." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Trouble shooted wireline winch spooling arm problem" "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Continued RIH from 264 m to 3162 m" "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Engaged GS pulling tool and released EVO plug. Waited for element to retract." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: POOH with GS tool/EVO plug on WL at 2200 m." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Continued POOH with GS tool/EVO plug on WL from 2200 m to surface." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: L/D WL tools and EVO plug. Rigged down sheaves." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed line test to 345 bar for 10 min." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged up cement line to string and tested Production Packer from below to 35/345 bar for 5/30 min." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3174m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Bled off pressure and rigged down cement hose and removed pump-in sub." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Backed out running tool and pulled landing string and L/D same to deck." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Rigged down casing equipment and control line equipment. Removed circulation sub from landing stand." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: P/U and M/U BPV and running tool. RIH on DP and sat BPV in Multibowl. POOH with RT on DP. L/D RT." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Drained Diverter, Overshot and BOP of brine." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Rigged up to pull Diverter to rig floor." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed hatches on rig floor for XMT. Rigged up in Moonpool for removing BOP." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled Diverter and slick joint to rig floor. Cleaned and placed on setback." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Disconnected NT-2 connector. Removed tension system." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lifted BOP and skidded to Stb side." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Drained riser spool and unbolted same." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed scaffolding from Moonpool." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled spool piece to rig floor and Layed out same." "On 2014-01-04, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Assisted at Multibowl with tuggers from rig floor. Removed scaffolding. Prepared WH for installation of spool and XMT. 2 of 3 control lines terminated." "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Prepared WH for installation of spool and XMT." "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed Tool Box talk for lift of Spool." "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed hatch" "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lifted down Spool" "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Continuing lifting down Spool and installed same on WH." "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Tested Spool piece to 35/345 bar for 5/15 min." "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Transfered XMT from moonpool crane to chains and lowered same down onto Spool. M/U same." "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 10.5 hours. Operational details: Tested Spool/XMT connection. Worked on control lines connections on WH. Installed elbow on XMT and flowline. Installed half moon. Simulatneously started to prepare for and rig up WL equipment." "On 2014-01-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed XMT lifing cap and installed Tree cap. Well handed over to Production at 24:00 hrs." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Well handed over to Production at 00:00 hrs. Meanwhile continued instrumentation work on XMT" "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.8 hours. Operational details: Production performing commisioning of XMT. Meanwhile finalized rigup for testing with cement unit and performed maintenance." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 8.8 hours. Operational details: Production performing commisioning of XMT. Meanwhile spotted WL BOP in moonpool and brought WL equipment to rig floor. Built riser and lubrictaor sections for WL." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held Tool Box talk with all involved personel for leak testing XMT." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Connected AWS test pump hose from WH panel" "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Performed line test from cmt unit to KWV, 20/345 bar for 5/15 min." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Filled XMT with Packer fluid and closed SV. Confirmed line from PWV vented. Tested XMT body to 30/345 bar for 5/15 min against BPV." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Inflow tested MMV to 250 bar for 15 min." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Inflow tested HMV to 250 bar for 15 min." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held Tool Box meeting" "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Opened HMV and closed KWV. Bled off pressure to 10 bar. Inflow tested KWV to 250 bar for 15 min." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed Tree Cap and retrieved Dart and BPV." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Connected control hoses to XMT." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed Tool Box talk before rigging up." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Installed lower spool onto XMT, removed lifting cap." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Installed lifing cap onto WL BOP. P/U WL BOP and installed on lower spool." "On 2014-01-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Connected control hoses to WL BOP and function tested same." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Continued to connect control hoses to WL BOP and function tested same." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Filled equipment with MEG" "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.8 hours. Operational details: Tested WL riser. Observed leak in Swab valve, applied back pressure and performed good test." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Held Tool Box talk" "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.5 hours. Operational details: Installed mid riser jont and M/U same. Made up grease head and installed WL into lubrator head." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Installed T-bar and upper sheave on elevator. Connected slings to lubracator head." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: P/U lubricator head" "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.2 hours. Operational details: Continued to P/U lubricator head" "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Installed lower sheave and M/U sinker bars. Spotted Slumb tool on rig floor." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Held Tool Box talk with ongoing shift." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: P/U weight bars and M/U lubricator." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.0 hours. Operational details: Tested line up to 345 bar. Tested WL lubricator and riser to 30/250 bar for 5/10 min." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.2 hours. Operational details: Broke out QTS and L/D weight bars." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Held Tool Box talk." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 5.5 hours. Operational details: Took WL head down for installation of toolstring. Tested same. P/U and M/U toolstring and guns. Tested same." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Tested QTS with test pump on rig floor to 30/250 bar for 5/10 min." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Opened MIV and filled riser and lubricator with MEG. Opened DHSV. Opened HMV." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3500m. The activity was categorized as 'completion -- perforate' and lasted for 4.0 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 3500 m / 73,2 deg inclination." "On 2014-01-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4300m. The activity was categorized as 'completion -- perforate' and lasted for 3.8 hours. Operational details: Continued RIH with perforation string on WL using Tractor." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4400m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: Continued RIH with perforation string on WL with Tractor from 4300 to 4400 m. Lost contact to Tractor." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4400m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Trouble shot communication to tractor (Production Electronics Cartridg )" "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4200m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Trouble shot communication to tractor (Production Electronics Cartridge)" "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: POOH with perforation string on WL from 4200 m. Bled down lubricator, closed XMT." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to break out lubricator and L/D tractor unit." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Broke out lubricator at QST. L/D tractor unit. Checked and tested new tractor system." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: P/U and M/U tool string." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U lubricator to QST and pressure tested connection to 30/250 bar for 5/10 min." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Filled lubricator and riser with meg via MIV 240 ltr. Opened DHSV. Opened HMV." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3500m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 3500 m / 73,2 deg inclination." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4400m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: RIH with perforation string on WL using tractor from 3500 m to 4400 m." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4570m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with perforation string on WL using Tractor from 4400 m to 4570 m. Observed high current on tractor. Experienced a lot of debris. Tractor can not push the gun after 4570m." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4600m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with perforation string on WL using tractor. Worked down from 4570 m to 4600 m." "On 2014-01-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4582m. The activity was categorized as 'completion -- perforate' and lasted for 4.0 hours. Operational details: Switched to passthrough mode. Started correlating tool string according to program. Max depth 4607 m. Performed first pass, second pass and third pass." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4594m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Correlated tool string according to program between 4582 m to 4594 m. Performed fourth pass and fifth pass up on depth." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4582m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure on well from 52 bar to 35 bar prior to firing guns." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4578m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Correlated to position guns at interval 1 from 4582 m to 4594 m. Firing depht 4578 m." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4578m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 4582 m to 4594 m with WHP 35 bar. WHP stabilized at 24,8 bar." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3750m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: POOH with perforation string on WL from 4578 m while performed G-ray/CCL logging to 3750 m." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: POOH with perforation string on WL from 3750 m. Powered down logging unit." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Tools in catcher. Closed SV, 9,8 bar SIWHP. Closed HMW." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to R/D lubricator and changing out tool string and L/O guns." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns. Checked and tested new tractor system." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 5.0 hours. Operational details: Performed test on tool string prior to P/U perforating run no. 2." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U guns, tool string and tractor." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 26m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: P/U guns, tool string and tractor for perforating run no. 2. M/U lubricator at QST." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 26m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Pressure tested lubricator to 250 bar. Filled riser with meg." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4100m. The activity was categorized as 'completion -- perforate' and lasted for 4.0 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 4100 m / 74,95 deg inclination." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4565m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: RIH with perforation string on WL using tractor from 4100 m to 4565 m. WHP increased from 23,9 bar to 110 bar." "On 2014-01-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4555m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Correlated across interval 4524 m to 4536 m. First pass." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4536m. The activity was categorized as 'completion -- perforate' and lasted for 6.0 hours. Operational details: Correlated across interval 4524 m to 4536 m. 9 th pass." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4536m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Correlated across interval 4524 m to 4536 m. 9 th pass." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4536m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 4524 m to 4536 m with WHP 15 bar. WHP stabilized at 25 bar." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: POOH from 4536 m to 230 m with perforating gun assembly no. 2. Powered down logging unit." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Tools in catcher. Closed SV, 9,8 bar SIWHP. Closed HMW." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to R/D lubricator and changing out tool string and L/O guns." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns. Checked and tested system." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 4.5 hours. Operational details: Change cable head and prepared guns for run no. 3." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U guns, tool string and tractor." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 12m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: P/U guns, tool string and tractor for perforating run no. 3." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 12m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Trouble shot communication to tractor. Changed out tractor unit." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: P/U guns, tool string and tractor for perforating run no. 3." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to complete and stab on lubricator." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator at QST. Pressure tested lubricator to 345 bar. Filled riser with meg." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 500m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: RIH with perforation string on WL to 500 m." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 500m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Performed test on tools. Lost communication to tools." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH from 500 m with perforation string on WL. Tools in catcher. Closed SV, 21,2 bar SIWHP. Closed HMW." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to break lubricator and check tool string." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Broke out lubricator at QST. Inspected and tested tool string firing head." "On 2014-01-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed firing head." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Checked firing head, crimped wire observed." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: M/U firing head to tool string. Function tested tool string." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U lubricator at QST. Pressure tested lubricator to 275 bar. Filled riser with meg." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Opened well and RIH with perforation string no. 3 on WL to 250 m." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4100m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 4100 m / 74,95 deg inclination." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4100m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Correlated across interval 4110 m to 4122 m." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4112m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Correlated across interval 4110 m to 4122 m. 5 th pass." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4112m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 4110 m to 4122 m with WHP 10 bar. WHP stabilized at 31 bar." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: POOH from 4112 m to 230 m with perforating gun assembly no. 3. Powered down logging unit." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 31 bar SIWHP. Closed HMW." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to R/D lubricator and changing out tool string and L/O guns." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 6.0 hours. Operational details: Cutted electric line and re-connected cable head, prepared guns for run no. 4. Aker performed pressure test on rig up 20/250 bar with dummy tool string." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 4.5 hours. Operational details: Worked on test tools and cable head. Checked and tested system." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U guns, tool string and tractor." "On 2014-01-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: P/U tractor and connected cabel head." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Performed system test on tractor. M/U lubricator at QST." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: P/U guns and tool string for perforating run no. 4." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator at QST. Pressure tested lubricator to 275 bar. Filled riser with meg." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Opened well and RIH with perforation string no. 4 on WL to 250 m." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4100m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 4100 m / 74,95 deg inclination." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4100m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Correlated across interval 4022 m to 4034 m." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 4022 m to 4034 m with WHP 32 bar. WHP stabilized at 32 bar." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 230m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: POOH from 4019 m to 230 m with perforating gun assembly no. 4. Powered down logging unit." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 32 bar SIWHP. Closed HMW." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to R/D lubricator and changing out tool string and L/O guns." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Performed test on cabel head." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Observed that the lubricator head suspension sling had caught up on elevator bolt. Performed pre-job meeting. Reslung lubricator head." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Serviced and inspected lubricator head. Inspected wire line upper sheave." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Performed test on tool string." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U perforating assy no. 5." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: P/U guns and tool string for perforating run no. 5." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator at QST. Pressure tested lubricator to 275 bar. Filled riser with meg." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Opened well and RIH with perforation string no. 5 on WL to 250 m." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4000m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 4000 m / 71,3 deg inclination." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3887m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: Correlated across interval 3890 m to 3902 m." "On 2014-01-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3887m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3890 m to 3902 m with WHP 32 bar. WHP stabilized at 32 bar." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: POOH from 3987 m to 250 m with perforating gun assembly no. 5. Powered down logging unit." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 33 bar SIWHP. Closed HMW." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to R/D lubricator and changing out tool string and L/O guns." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Prepared guns for run no. 6 on deck." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.2 hours. Operational details: Prepared guns for run no. 6 on deck. Tested tool string." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW. Wind speed above 40 knts. Cranes unavailabel for handling tool string. Performed pre-job meeting prior to P/U perforating assy no. 6." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: L/O tool string from run no. 5. P/U guns and tool string for perforating run no. 6." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator at QST. Pressure tested lubricator to 250 bar. Filled riser with meg." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Opened well and RIH with perforation string no. 6 on WL to 250 m." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4045m. The activity was categorized as 'completion -- perforate' and lasted for 4.0 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program to 4045 m. Toolstring stopped moving at 3700 m / 79 deg inclination. Used tractor from 3700 m to 3800 m." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3859m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: Correlated across interval 3853 m to 3859 m." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3859m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3853 m to 3859 m with WHP 33,8 bar. WHP stabilized at 33 bar." "On 2014-01-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1000m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: POOH from 3859 m to 1000 m with perforating gun assembly no. 6." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: POOH from 1000 m to 250 m with perforating gun assembly no. 6. Powered down logging unit." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 42 bar SIWHP. Closed HMW." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to R/D lubricator and changing out tool string and L/O guns." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Prepared guns for run no. 7 on deck." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Prepared guns for run no. 7 on deck. Tested tool string." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U perforating tool string no. 7." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: P/U guns and tool string for perforating run no. 7." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: M/U lubricator at QST. Pressure tested lubricator to 250 bar. Filled riser with meg." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3620m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 3620 m / 77,6 deg inclination." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4100m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Continued RIH with perforation string on WL using Tractor to 4100 m" "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3831m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Correlated across interval 3825 m to 3831 m." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3822m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3825 m to 3831 m with WHP 33,8 bar. WHP stabilized at 33 bar." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: POOH from 1000 m to 250 m with perforating gun assembly no. 7. Powered down logging unit." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 42 bar SIWHP. Closed HMW." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 3.8 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to R/D lubricator, tool string and L/O guns." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns." "On 2014-01-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.2 hours. Operational details: R/D wire line equipment. B/D lubricator and L/D same on deck." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: R/D wire line equipment. B/D lubricator and L/D same on deck." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared drill floor for exccess wire line equipment." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.8 hours. Operational details: R/D wire line equipment. Disconnected top riser and removed wire line BOP." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: R/D wire line equipment. Removed spool and riser joint from x-mas tree." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Installed half moon on F-15 and secured same." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.2 hours. Operational details: Flushed lines with 1 m3 packer fluid" "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Installed tree cap and needle valve on xmas tree." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Started to pressure test x-mas tree, DHSV, MMV and HMV. according to procedure." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 3.8 hours. Operational details: Bullheaded 3 m3 100 % meg, 6,6 m3 packer fluid and 1,2 m3 100 % meg." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.8 hours. Operational details: Performed inflow test on DHSV, MMV and HMV." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: R/D chicksan lines and valves from x-mas tree." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Pressure tested x-mas tree cap to 250 bar." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Cleared well head area for excces equipment." "On 2014-01-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Prepared and handed over well to production. Await decision for F-1 operation. Operation completed continued operation on 15/9 F-99. Await decision for F-1 operation." "On 2015-08-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 6.5 hours. Operational details: Vessel arrived rig. Spotted equipment in work area on pipedeck. Prepared equipment and checked inventory." "On 2015-08-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Personnel arrived rig." "On 2015-08-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Continued to prepare equipment on pipedeck" "On 2015-08-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held brief with platform management for day and night shift." "On 2015-08-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Continued to prepare equipment on pipedeck" "On 2015-08-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Held start up meeting regarding well operation with all involved personnel." "On 2015-08-05, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Electrican hooked up wireline units and logging-cabin to rig power and Fire & Gas" "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Continued to hook up units to rig power and Fire & Gas. Meanwhile prepared hoses for BOP test and chicksan for XMT." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 4.0 hours. Operational details: Function tested BOP. Leak tested same on stump to 345 bar. Meanwhile changed well hatch to wireline hatch in moonpool." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Function tested wireline winch and spooled out cable." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT for building GIH." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Started to build GIH." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Performed start up meeting for operation with dayshift." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Continued to build GIH and threaded cable through same." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: Spotted W/L grease and RX72 to drill floor. Rearranged equipment on pipedeck and completed Z-015 checklist. Meanwhile prepared BOP for lifting." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Lifted BOP down to wellhead area and riser pieces to drill floor." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Well handed over from production to D&W. Meanwhile: Build lubricator and riser horizontally on drillfloor." "On 2015-08-06, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.0 hours. Operational details: Rigged up chiksan lines on XMT kill wing manifold. Hooked up Altus pump skid for local control of DHSV and HMV." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Hooked up equalizing loop from SWV to PW. Leak tested SW manifold to 20/345 bar for 5/10 min." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Removed top cap from XMT and installed lower riser." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installation of wireline BOP" "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Moved BOP into position and installed BOP onto lower riser." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Installed hydraulic control hoses onto BOP. Function tested and performed visual connection test on lower riser and BOP against SV to 345 bar for 5 min." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to P/U riser." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: P/U riser and connected onto BOP. Installed QTS onto riser stick up. Changed elevator inserts and installed T bar and wireline sheave." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Prepared lubricator and hooked up GIH hoses. Meanwhile: Recieved remaining equipment from supply vessel. (SLB gun basket and container)" "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for testing C/L to DHSV and HMV." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.4 hours. Operational details: Tested C/L to DHSV and HMV to 520 bar. Hooked up N2 bottle rack for emergency air supply to grease skid. Meanwhile: Checked counter wheel on W/L winch. Secured hoses on lubricator. Meanwhile: Schlumberger tested perforation tools and L/D guns on pipe deck." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Prepared lubricator for lifting." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for lifting and installation of lubricator." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: Lifted lubricator for installation on top of riser. Stopped lifting operation due to challenges to maneuver lubricator by using tugger." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.3 hours. Operational details: Peformed TBT for lifting lubricator and installing tractor." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Lifted lubricator on top of riser. Had to use rig crane to assist lift." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Hooked up closed drain hose on wellhead. Meanwhile: Built toolstring for lubricator leak test. Filled lubricator with MEG." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Installed tractor in lubricator and leak tested rig up to 20/345 bar for 5/10 min. Leak tested bleed off line to 20/150 bar for 5/10 min." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Bled off lubricator, purged lubricator with N2 and drained MEG in riser to closed drain." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Peformed TBT prior to disconnecting lubricator and L/D toolstring." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Disconnected lubricator and L/D toolstring." "On 2015-08-07, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: Schlumberger tested logging tools and Altus tractor." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Continued testing Schlumberger and Altus BHA. Discovered issue with compatabilty between Altus voltage protector module (VPM) and Schlumberger GR/CCL logging module." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Evaluated situation. Discussed different options." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Altus and Schlumberger rearranged toolstring and tested different options. Decided to run single logging run without perf.guns." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U logging BHA." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.1 hours. Operational details: M/U BHA for run # 1 (3 1/8'' tractor and GR/CCL). Added 40 litr Ramex 50/50 MEG in riser. Leak tested lubricator/QTS to 20/345 bar 5/10 min." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.9 hours. Operational details: Equalized and opened HMV and pumped MEG for equalizing DHSV. Opened DHSV. WHP 68 bar. Equalized and opened SV with 43 turns." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3500m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: RIH w/BHA #1 by gravity from 0 m to 3500 m, WHP 68 bar. Toolstring stopped at 3500 m. Depth: P/U Weight: 500 m 1020 lbs 1000 m 1475 lbs 1500 m 2070 lbs 2000 m 2740 lbs 3000 m 3750 lbs 3500 m 4000 lbs Friction factor calculated to 0,25. Held well control drill after DHSV was passed and verified open: Leak in GIH." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3900m. The activity was categorized as 'interruption -- other' and lasted for 0.9 hours. Operational details: RIH with tractor activated from 3500 m to 3900 m. Stopped at logging depth." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3850m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Started to POOH to perform GR/CCL logging. Had to stop after 50 m due to noice from W/L winch drum." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3850m. The activity was categorized as 'interruption -- other' and lasted for 2.7 hours. Operational details: Adjusted W/L drum position." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3650m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Continued to POOH for 200 m while logging GR/CCL. Observed same noice from W/L drum." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3650m. The activity was categorized as 'interruption -- other' and lasted for 1.3 hours. Operational details: Called out mechanic. Was able to adjust W/L drum to correct position. Continued to POOH while logging." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3348m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Continued to POOH while logging GR/CCL from 3650 m to 3348 m. POOH." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.7 hours. Operational details: POOH with BHA#1 from 3348 m to surface. WHP 69 bar. Meanwhile PETEC verified GR/CCL correlation log OK." "On 2015-08-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Closed SV & HMV and inflow tested same. Bled off lubricator and purged R/U with N2 to closed drain." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.4 hours. Operational details: Continued to drain lubricator to closed drain." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to L/D toolstring." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Broke lubricator and L/D tractor and GR/CCL." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.7 hours. Operational details: Schlumberger and Altus checked compatibility issue." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Schlumberger and Altus performed hot check for perforation run #1." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT prior to M/U tractor and perforation guns." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: M/U BHA #2 for perf. run #1." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for dayshift." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Continued M/U BHA #2 (3 1/8'' tractor and 4,5'' perf.guns). Added 30 litr Ramex 50/50 MEG in riser. Leak tested lubricator/QTS to 20/345 bar 5/10 min." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3521m. The activity was categorized as 'workover -- perforate' and lasted for 3.2 hours. Operational details: RIH w/ BHA #2 ' by gravity from 0 m to 3521 m. WHP 71bar. Depth: P/U Weight: 500 m 2700 lbs 1000 m 3300 lbs 1500 m 4050 lbs 2000 m 4800 lbs 2500 m 5650 lbs 3000 m 5400 lbs 3500 m 5400 lbs" "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3521m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Correlated across pup at 3472 m." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3565m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Continued RIH w/ BHA #2 from 3521 m to 3565 m. Toolstring stopped." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3592m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: RIH with tractor activated from 3565 m to 3592 m. Lost communicaton with tractor." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3592m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshooted tractor. Not possible to activate tractor. Decided to POOH." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3355m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH from 3592 to 3355 m. Add-on drum turned and came out of position and damaged cable." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3355m. The activity was categorized as 'interruption -- other' and lasted for 0.7 hours. Operational details: Inspected cable and found wire strand damaged." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3355m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Time out and evaluated situation. Aligned and secured Add-on drum." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.4 hours. Operational details: POOH from 3355 m to surface. WHP 72 bar. Closed SV & HMV and inflow tested same. Bled off lubricator and purged R/U with N2 to closed drain. Meanwhile mobilised new cable from onshore." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/D toolstring and lubricator." "On 2015-08-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Broke lubricator. L/D BHA on deck. L/D lubricator on catwalk. Spoled back cabel to winch." "On 2015-08-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Not able to continue operation with cable. Had to order new cable from onshore. Meanwhile: Checked tractor failure. Cleaned drill floor. Prepared Add-on drum to be shipped onshore." "On 2015-08-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Waited on new cable from onshore." "On 2015-08-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 12.0 hours. Operational details: Waited on new cable from onshore." "On 2015-08-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Waited on new cable from onshore." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Waited on new cable from onshore. Meanwhile: Performed well control drill with service companies involved in operation." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Waited on new cable from onshore." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.3 hours. Operational details: New Add-on drum arrived on rig. Hooked up Add-on drum to WL winch. Evaluated the need to cut of cable from drum due to high resistance on cable. Meanwhile: Checked tractor on deck." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.3 hours. Operational details: Waited on 'green light' form onshore to cut cable." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Positioned Add-on container for spooling of cable. Connected Add-on drum and spooled of 1586 m cable into skip." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Repositioned Add-on drum and hooked it up." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Threaded cable through GIH." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Built cable head. Meanwhile: Secured Add-on drum with tie-down chains. Held TBT on rig floor prior to P/U lubricator." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.1 hours. Operational details: Function tested tractor and Schlumberger tested CCL and firing system." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.2 hours. Operational details: P/U lubrictor and installed toolstring for leak test. Filled lubricator with MEG and leak tested same to 20/345bar 5/10 min." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for disconnect lubricator and M/U BHA#3 for perf.run #1." "On 2015-08-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Disconnected lubricator and M/U BHA#3 for perf.run #1. Added 30 litr Ramex 50/50 MEG in riser." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Leak tested QTS to 20/345 bar 5/10 min. Equlized SV and HMV using MEG. WHP 75 bar." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3390m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: RIH w/BHA #3 by gravity from 0 m to 3390 m, WHP 75 bar. Toolstring stopped at 3390 m. Depth: P/U Weight: 400 m 3200 lbs 1200 m 4100 lbs 2000 m 5500 lbs 2800 m 6600 lbs 3200 m 6200 lbs Friction factor 0,25." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3520m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: RIH with tractor activated from 3390 m to 3520 m." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3442m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Correlated from 3520 m across pup joint at 3472 m at 10 m/min. Stopped at 3442 m. Activated tractor." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3810m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Tractored down at 10 m/min from 3442 m to 3810 m." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3810m. The activity was categorized as 'workover -- perforate' and lasted for 2.2 hours. Operational details: Performed correlation, 5 passes in interval 3810 m to 3708 m, used tractor when RIH." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3772m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: P/U at 10 m/min to 3743 m CCL depth. Bottom BHA at 3772 m Placing top shot at 3748 m and bottom shot at 3766 m. HW 5880 lbs. WHP 75,1 bar. BHP 281 bar." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3772m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Perforated well in interval 3748 m to 3766 m. WHP increased to 79 bar and BHP increased to 285 bar." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3572m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: POOH at 10 m/min and logged CCL up to 3572 m." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 1.4 hours. Operational details: Continued POOH to 500 m. Prepared for handling explosives on surface." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: POOH to surface." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: OOH, closed SV and HMV inflow tested same. Bled of pressure in R/U to closed drain. Flushed R/U with N2." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.8 hours. Operational details: Disconnected lubricator. Production measured benzene to > 10 ppm inside riser and 0 ppm outside riser. L/D BHA#3." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.7 hours. Operational details: Prepared tools for BHA#4 for perf.run#2." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Observed gas in cablehead, megging not satisfied. Had to ventilate gas out of cable." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: Performed Altus / Schlumberger tractor check." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for R/U toolstring." "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.9 hours. Operational details: R/U toolstring perf.run#2. Added 40 litr Ramex 50/50 MEG in riser. Leak tested QTS to 20/345 bar 5/10 min. Equlized SV and HMV using MEG. WHP: 79 bar" "On 2015-08-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 700m. The activity was categorized as 'workover -- perforate' and lasted for 1.1 hours. Operational details: RIH w/BHA #4 (3 1/8'' tractor and 4 1/2'' perf.guns) by gravity from surface to 1200 m." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3392m. The activity was categorized as 'workover -- perforate' and lasted for 2.1 hours. Operational details: Continued RIH by gravity from 1200 m to 3392 m, WHP 79 bar. Toolstring stopped at 3392 m. Depth: P/U Weight: 400 3200 lbs 800 3700 lbs 1200 4100 lbs 1600 4950 lbs 2000 5500 lbs 2400 6300 lbs 2800 6600 lbs 3200 6200 lbs Friction factor 0,19" "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3610m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: RIH with tractor activated from 3392 m to 3610 m. Average running speed 15 m/min." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3610m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: Performed 3 orientation passes from 3610 m - 3450 m. Used tractor when RIH" "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3552m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Correlated across interval 3610 - 3450 m. Positioned gun with top shot at 3540 m and bottom shot at 3552 m. WHP 79 bar. BHP: 285.5" "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3540m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Perforated well in interval 3540 m to 3552 m. WHP increased to 82,5 bar and BHP increased to 289 bar." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3300m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: POOH with perf.run#2 from 3540 m to surface at 30 m/min." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Continued POOH to surface." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: OOH, closed SV and HMV. Inflow tested HMV. SIWHP 81 bar." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Bled of pressure in lubricator and purged R/U with N2 to closed drain." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.7 hours. Operational details: Disconnected lubricator and L/D BHA #4 (3 1/8'' tractor and 4 1/2'' perf.guns). All shots fired." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: Spooled out cable. Altus tractor checked BHA components." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.1 hours. Operational details: Built new cable head. Performed torsion test on cable: Had more than 10 turns, cable OK." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Function tested BHA on deck, had some problems with telemetri. Altus not able to communicate with tractor." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Altus tractor troubleshoted communication problems with tractor. Altus tractor re-started surface equipment and function tested OK." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: Tested toolstring for perf.run#3 and checked equipment according to Schlumberger check list." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for M/U BHA#5 for perf.run#3" "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: M/U BHA#5 for perf.run#3. Added 30 liter Ramex and 50/50 MEG." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Leak tested QTS to 20/345 bar 5/10 min. Equlized SV and HMV using MEG. WHP 83 bar." "On 2015-08-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- perforate' and lasted for 2.2 hours. Operational details: RIH w/BHA#5 (3 1/8'' tractor and 4 1/2'' perf.guns) by gravity from surface to 2800m." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3408m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Continued RIH by gravity from 2800 m to 3408m, WHP 83 bar. Toolstring stopped at 3408 m. Depth: P/U Weight: 400 2550 lbs 800 2950 lbs 1200 3500 lbs 1600 4100 lbs 2000 4700 lbs 2400 5400 lbs 2800 5200 lbs 3200 5300 lbs 3407 5300 lbs Friction factor 0,22" "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3560m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: RIH with tractor activated from 3408 m to 3560 m." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3545m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Performed 3 orientation passes from 3545 m - 3450 m. Used tractor when RIH." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3503m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Correlated across interval 3545 m - 3450 m. Positioned gun with top shot at 3508 m and bottom shot at 3517 m WHP 83 bar. BHP 289,5 bar." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3503m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Perforated interval 3508 m - 3518 m. WHP increased to 86 bar. BHP increased to 293 bar." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.7 hours. Operational details: POOH from 3503 m to surface. Average pulling speed 30m/min." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: OOH, closed SV and HMV. Inflow tested HMV. SIWHP bar 86 bar." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.4 hours. Operational details: Bled of pressure in lubricator and purged R/U with N2 to closed drain." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for disconnecting lubricator and L/D toolstring." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: Disconnected lubricator and L/D BHA #5 (3 1/8'' tractor and 4 1/2'' perf.guns). All shots fired." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Spooled out cable. Altus tractor checked BHA components." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.8 hours. Operational details: Altus tractor and Schlumberger function tested equipment and prepared toolstring for next run. Meanwhile: Tested cable head." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: M/U BHA#6 for perf.run#4. Added 40 liter Ramex." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Leak tested QTS to 20/345 bar 5/10 min. Equlized SV and HMV using MEG. WHP 86 bar." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3310m. The activity was categorized as 'workover -- perforate' and lasted for 2.8 hours. Operational details: RIH w/BHA#6 (3 1/8'' tractor and 4 1/2'' perf.guns) by gravity from surface to 3310 m. WHP 86 bar. Toolstring stopped at 3310 m. Depth: P/U Weight: 400 2530 lbs 800 3100 lbs 1200 3450 lbs 1600 4040 lbs 2000 4530 lbs 2400 4800 lbs 2800 5300 lbs 3200 5600 lbs 3407 4800 lbs Friction factor 0,21" "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3535m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: RIH with tractor activated from 3310 m to 3535 m. Average running speed 12 m/min." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3535m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Performed 3 orientation passes from 3540 m to 3435 m. Used tractor when RIH." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3477m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Correlated across interval 3540 to 3435 m. Positioned gun with top shot at 3483 m and bottom shot at 3491m. WHP 86 bar. BHP: 293,5 bar." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3477m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Perforated well in interval 3483 m to 3491 m. WHP increased to 87 bar and BHP increased to 294 bar." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.3 hours. Operational details: POOH with perf.run#4 from 3477 m to surface at 30 m/min." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: OOH, closed SV and HMV. Inflow tested SV and HMV. SIWHP 87 bar." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Bled of pressure in lubricator and purged R/U with N2 to closed drain." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for L/U toolstring and lubricator." "On 2015-08-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Disconnected lubricator and L/D BHA#6 (3 1/8'' tractor and 4 1/2'' perf.guns). All shots fired." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: Continued L/D toolstring and lubricator. WHP 87 bar." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.5 hours. Operational details: Closed BOP and DHSV and bled down to 5 bar above DHSV. WHP when closing DHSV: 87 bar. BHP: 294 bar. Inflow tested DHSV for 30 min with 87 bar below and 5 bar above. Pressure above DHSV increased 0,3 bar/30 min. Closed HMV. Meanwhile: R/D Altus W/L, tractor and Schlumberger peforation equipment." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.8 hours. Operational details: Continued to R/D Altus W/L, tractor and Schlumberger peforation equipment." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Disconnected chiksan on wellhead. Disconnected and lifted BOP to drill floor." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 3.0 hours. Operational details: Installed and leak tested XT top cap 5/10min 20/345bar. Leak tested KWV cap 5/10min 20/345bar." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: R/D and prepared W/L equipment for backload." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Handed well over to production." "On 2015-08-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 8.0 hours. Operational details: R/D and packed W/L equipment." "On 2015-08-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Cleaned drillfloor and moonpool area." "On 2015-08-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Cleaned pipedeck. ********************************************** Ended operation on well ************************************" "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 4.8 hours. Operational details: Prepared for skidding from well F-1C to well F-15D: deck, cantilever, moonpool. Performed TBT prior to skidding. Carried out last preparations prior to skid. Removed stairs to cantilever. Skidded cantilever." "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Stopped skidding due to burst hose on skid cylinder. Changed same." "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Continued skidding cantilever onto F-15D well" "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Re-installed stairs on cantilever" "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed daily maintenance on the drill floor. Respooled rig floor tugger. Started working on changing out slew motor on aft PRS" "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Prejob meeting for stripping annular BOP for inspection. Prejob meeting for rigging up at XT deck. Worked on changing out slew motor on aft PRS" "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued working on annular BOP and rigging up bleed off manifold on XT deck. Worked on changing out slew motor on aft PRS" "On 2016-07-08, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Removed cap and annular element, cleaned surface and replaced adaptor ring. Worked on changing out slew motor on aft PRS" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued working to replace adapter ring on annular BP. Found hard cement around annular BOP. Meanwhile worked on replacing slew motor on aft PRS. Pressure tested bleed of manifold on XT deck 20bar/5 min, 345bar/10 min. Connected hose and filled A-annulus and B-annulus with water." "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued working on BOP and PRS. Errected scaffolding above choke manifold. Worked to connect hydraulic pump to locally control DHSV and HMV" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued working on BOP adaptor ring. Test run PRS. Carried out TBT for pressure testing rig floor manifolds. Worked to pressure test rig floor manifolds. Prepared rig floor to lay out 7in tbg from the derrick" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Attempted to instal adaptor ring, not able to land out all the way, 3.5cm short. Pulled adaptor ring. Started to lay out 7in tbg from the derrick. Worked to pressure test rig floor manifolds" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Rig power system shutdown due to turbine issues" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.8 hours. Operational details: Installed adaptor ring, installed annular BOP. Worked to lay out 7in tbg from the derrick, worked to pressure test rig floor manifolds. Cleaned and cleared BOP after re-building annular. Alarm went on on primary cooling pump for cabinets (cement unit equipment). Inspected cooling pump, confirmed leak, switched cabinets cooling system to backup." "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: TBT to remove hatch on F-15 and instal half-moon hatch" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Lowered down 2x half-moon hatches from moon. Removed hatch on F-15 and lifted hatch up into moon pull. Installed half-moon hatches over well F-15. Double secured lifts." "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: TBT for handling and preparing cement spool" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lifted up cement spool and shifted load from 35t cranes to 2x 6t rig floor tuggers. Double secured lifts" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lowered down cement spool onto XMT and M/U same using BX156 seal ring" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Installed hole covers and tarpoulin in moonpool. Performed TBT w/ scaffolders. Built scaffolding around cement spool. Meanwhile worked on housekeeping in moonpool and carried out TBT for pressure test cement spool" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Lined up and flushed from cement unit to cement spool. Pressure tested cement spool to 20/345 bar for 5/10min. Good test." "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting before bulheading operation. Meanwhile started greasing XT valves" "On 2016-07-09, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Confirmed line up from mud pumps, meanwhile continued greasing valves and added surfactant into wash pill" "On 2016-07-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Finished with greasing valves, opened hydraulic master valve, verified no pressure, opened swab valve, opened DHSV" "On 2016-07-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Pumped into the well 3m3 50/50 mix of MEG and sea water, 5 bar, 10m3 wash pill, pressure equalised at 58 bar above DHSV. Continued pumping sea water. Pressure 60-80 bar, 1300l/min. Pressure gradually increased to 150bar. After 180m3 pumped (2x well volumes) shut down pumps. Monitored SIWHP for 20 min. Pressure down to 24 bar." "On 2016-07-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 5.0 hours. Operational details: Continued bullheading into the well w/ 1300l/min, pressure stabilized at 170bar, slowly decreasing to 165 bar. After 360m3 pumped (4x well volumes) shut down pumps. Monitored SIWHP for 15 min. Pressure down to 48 bar." "On 2016-07-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 6.2 hours. Operational details: Continued bullheading into the well w/ 1300l/min, pressure stabilized at 175bar, slowly decreasing to 170 bar. After 630m3 pumped (7x well volumes) shut down pumps. Monitored SIWHP for 15 min. Pressure down to 60 bar. Meanwhile evaluated situation, discussed w/ duty team onshore." "On 2016-07-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Continued bullheading into the well w/ 1300l/min, pressure stabilized at 182bar. Meanwhile carried out TBT for cementing operation. After 200m3 pumped (2,2x well volumes) shut down pumps. Monitored SIWHP. Pressure down to 95 bar. Confirmed w/ duty team onshore and continued with cementing operation. Totally bullheaded into the well 1370m3" "On 2016-07-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Released bottom dart. Mixed and pumped 27.6m3 of 1.9sg cement slurry at 800l/min. Pressure 116 bar, decreasing to 40bar, indicating cement moving down in the tubing. Displaced lines w/ 0,9m3 of Hi-vis pill. Released top dart. Pumped 7,1m3 of Hi-vis (totally pumped 8m3 of Hi-vis). Displaced w/ 50,4m3 of sea water at initial rate of 1200lpm. Pressure gradually increased to 150bar and then rapidly increased to 260bar, indicating plugging off perforation w/ cement slurry. Started reducing pumping rate in steps to keep pumping pressure below 270 bar. Reduced rate from 1200l/min to 170l/min. Pumped 3m3 of contamination pill, pressure at 260bar. Shut down pumps and monitored WH pressure decline. Recorded final stabilized squeeze pressure of 40bar. Closed swab valve. Verified volumes pumped by checking volumes left in the pits and silos. Theoretical top of cement 3172mMD. DHSV was cycled several times after 35m3 of sea water displacement was pumped" "On 2016-07-10, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: Continued laying down pipe. Meanwhile WOC. Worked on BOP tests" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 7.5 hours. Operational details: Layed out 7in tbg from derrick. Pressure tested BOP. Carried out maintenance on both PRSs. Continued monitoring WH pressure on XT gauge. As pressure increased from 40 bar (final squeeze pressure) to 60 bar due to temperature effect it was bled off back to 40bar. Had to bleed off several times. Cycled HMV and MMV valves on XT every 1 hour. Meanwhile WOC" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting for pressure testing and inflow testing cement plug and DHSV. Continued monitoring WH pressure on XT gauge." "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Performed line test, rigged up bleed off line from cement unit to closed drain" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Closed HMV and bled off pressure between HMV and swab valve. Opened SV and equalized pressure above HMV according to final pressure on XT gauge of 51bar" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Opened HMV and increased pressure in tubing to 320 bar with SW using cement unit. Closed SV and performed cement plug pressure test to 320 bar/10 min. 763liters pumped from 51bar to 320bar." "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Carried out inflow test of cement plug. Bled down pressure in tubing through bleed valve to closed drain to 30 bar. Monitored pressure for 10 min. Slowly increasing. Bled down pressure in tubing to 20 bar. Monitored pressure for 10 min. Slowly increasing. Bled down pressure in tubing to 10 bar. Monitored pressure. Pressure steadily increased 11 bar/1 hour. Bled off from 21 bar to 10 bar. Monitored pressure for 30 min. Pressure increased 4.5 bar with clear decreasing trend towards the end. Good inflow test." "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Carried out inflow test of DHSV. Equalized pressure and opened swab valve and applied 310 bar to tubing. 830l pumped. Closed DHSV. Bled off pressure in tubing above DHSV to 240 bar. Checked pressure on DHPG to confirm DHSV is closed. Ok. Monitored pressure above DHSV for 30 min for 70bar LP inflow test. Pressure increased 2.5bar in 30 min with decreasing trend towards the end. Good LP inflow test. Bled down pressure in tubing above DHSV to 10bar. Checked pressure on DHPG to confirm DHSV is closed. Ok. Monitored pressure above DHSV for 30 min for 300bar HP inflow test. Pressure increased 2bar in 30 min with decreasing trend towards the end. Good HP inflow test. Equalized pressure above DHSV, pressured up control line to DHSV to 520bar to open DHSV. Bled off tubing pressure" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for rigging down cement spool." "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Started to rig down cement spool. Observed light fluid flow from KWV side of XT. Evaluated situation and concluded to trap 20bar under DHSV to have a differential across DHSV. Reconnected hose and swivel to cement spool. Confirmed line up. Pressured up tubing to 20bar. Bled off pressure above DHSV to 0 bar. Confirmed with DHPG that DHSV closed. 20bar differential pressure from below. Flow checked the well on KWV. Stable." "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Rigged down cement spool. L/D cement spool in moonpool" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to instal BPV and XT cap" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Lowered BPV on tugger into XT and landed BPV in tubing hanger. Installed XT cap" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Disconnected hydraulic hoses and lines from XT" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed scaffolding on XT deck, meanwhile performed TBT to remove hatches in moonpool" "On 2016-07-11, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed hatches on F-15 and F-10 in moonpool" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed hatches over F-15 and F-10 slots." "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Prepared XT and TDS for lifting operation. Carried out TBT to lift XT and pull foxhole" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Pulled foxhole to free up way for moonpool overhead crane for transporting XT" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled Master bushing. Attached lifting arrangement to XT as per lifting plan" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Removed Grayloc clamp below XT block. Lifted XT to moonpool and moved to transport skid, secured same on transport skid. Meanwhile installed hatch over F-10 slot to minimize openning" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed foxhole" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Removed half moon hatches on XT deck, released NT-2 connector. Lifted NT-2 bonnet and spacer spool to rig floor. L/D same" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Cut control lines in multibowl. Installed blank plug on exit blocks. Removed antivibration ring" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Lowered communication collar from moonpool to multibowl. Installed communication collar. Meanwhile errect scaffolding in moonpool." "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meetingto run HP riser" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Run HP riser, installed gasket, made up riser connection. R/D HP riser slings and recover chains to rig floor" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed moonpool hatches" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 6.0 hours. Operational details: Removed protector and cleaned seal face. Installed gasket. Landed BOP onto riser. Started working with tensioners. Meanwhile pressure tested choke manifold." "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Started to M/U NT-2 connector. Continued pressure test choke manifold" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed slick joint" "On 2016-07-12, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Continued to M/U NT-2 connector. Installed BOP tension system. Shifted BOP load to tension system" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed diverter" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: M/U bolts on slick joint. Meanwhile installed master bushing, performed TBT for pressure testing of riser connections" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Filled riser and BOP w/ sea water" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Tested riser connector to 20/310 bar for 5/10 min. Good test" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull BPV" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: M/U BPV retrieving tool to stand of 3,5in DP" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Pulled BPV dart to the rig floor" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Pulled BPV to the rig floor. L/D BPV retrieving tool" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to instal THRT" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Rigged up 7in tbg handling equipment" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U top 7in tbg joint and M/U to Weco 1502 swedge. L/D same" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U and RIH THRT" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U and M/U tubing hanger running tool, joint #2 and joint #3. Connected control lines" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Engaged THRT and took 2.5ton overpull test. Ok" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U cement line to swedge and tested same to 100bar. Ok" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pressured up control line to DHSV to 520bar. Pressured up above DHSV to 100bar w/ cement unit. DHSV did not open. Bled off pressure above DHSV. Closed LTV and retested line from cement unit to 250bar. Ok. Pressured up above DHSV to 120bar, DHSV opened. Bled off pressure from the well. Rigged down cement hose and LTV" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U WL" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U wireline equipment" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1500m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH w/ run #6, 5,375' OD cutter from 0 m to 1500 m. Average running speed 25 m/min" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2500m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH w/ run #6, 5,375' OD cutter from 1500 m to 2500 m. Average running speed 33 m/min" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3086m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH w/ run #6, 5,375' OD cutter from 2500 m to 3086 m. Average running speed 13 m/min" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3086m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Logged from 3086m to 2923m. RIH back to 3086m. Attempted to pass 3086m, no-go" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3086m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3075m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Positioned cutter at 3075 m . Performed cut. Observed 200l backflow at rotary" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: POOH from 3075 m to 0 m . Average pulling speed 34 m/min" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D wireline equipment" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U swedge, connected hose and LTV. Confirmed line up" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Staged up to 1300l and circulated 75m3 of sea water. Took returns from A-annulus through AKV and MGS to the dedicated slop pit. Max gas in returns 3%" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull TH" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/D cementing hose and broke off swedge" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Released TH w/ up weight 188t, no overpull. Bled off pressure in DHSV control line. Pulled and L/D landing string and THRT" "On 2016-07-13, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Started to change handling equipment. Removed master bushing, installed spider, installed pwer rollers, installed reel for spooling control line" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3075m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Changed handling equipment. Removed master bushing, installed spider, installed power rollers, installed reel for spooling control line" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2957m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Pulled tubing from 3075m to 2957m. Removed control line clamps, spooled control line, L/D tubing joints. Average pulling rate 4 joints/hour" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2957m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Experienced communication problems w/ csg tong. Changed door sensor" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2874m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Pulled tubing from 2957m to 2874m. Removed control line clamps, spooled control line, L/D tubing joints. Average pulling rate 7 joints/hour" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2874m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Experienced communication problems w/ csg tong" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2685m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Pulled tubing from 2874m to 2685m. Removed control line clamps, spooled control line, L/D tubing joints. Average pulling rate 6,4 joints/hour" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2685m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: HTS belt fault occurred, contacted electronics technician" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled tubing from 2685m to 2614m. Removed control line clamps, spooled control line, L/D tubing joints. Average pulling rate 6,0 joints/hour" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to rig down csg handling equipment" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pull slips" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled and L/D DHSV" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled tbg joint, removed control lines and run joint back into hole" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed out handling equipment to 5,5in DP" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleared rig floor" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U swedge to tubing" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2574m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D control line reel, meanwhile disconnected hoses and made csg tong ready to remove" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2585m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U single and RIH from 2574m to 2585m" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2585m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pulled master bushing and installed PS21" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3070m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: Continued RIH on 5,5in DP from 2585m to3070m. Filled pipe half way. Average RIH speed 214 m/hour." "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3070m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U TDS and staged up pumps to 3000l/m, 180 bar. Pumped 32m3 sea water and 20m3 wash pill, displaced combination wiper plug out of tbg (at 3070m)" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 3070m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.5 hours. Operational details: M/U side entry sub assembly. Performed Pre-job Meeting for cement job. Installed cement line and pressure tested same to 300bar. Ok" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2868m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Balanced cement plug (250m) Mixed and pumped 9,2 m3 of 1,9SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 2890 l of drill water. Zeroed volume counters. Displaced the cement with 45,6 m3 (2059 strokes) of sea water, 2000 l/min/ 65 bar. Pulled out of cement to 2868m (200m of cement)" "On 2016-07-14, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2868m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Circulated out upper 50m of cement at 2700l/min, pressure went from 185bar down to 140bar as cemented was circulated out of well. Observed cement returns on surface. Theoretical volume of returned cement was 1.8m3. Totally circulated 270m3. TOC at 2868m" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2832m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pulled 1x stand of DP, M/U BOP cleaning tool. Dropped 2,125in ball to function tool. Sheared at 50bar" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2832m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Flushed BOP, made 4x passes across BOP, circulated at 3500l/min, 20bar" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 4.0 hours. Operational details: POOH 5,5in DP from 2832 m to 2570 m . Had to pump out as excessive fooaming occured in the trip tank. R/U csg handling equipment." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U csg handling equipment" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling remaining tubing" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued R/U csg handling equipment" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2510m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: POOH with tubing from 2570 mMD to 2510 mMD. Cut control lines. Average pulling speed 4 jnts/hr." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2510m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Repaired sensor on casing tong. Meanwhile: Performed housekeeping on drill floor." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2280m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Continued POOH with tubing from 2510 mMD to 2280 mM. Average pulling speed 7,2 jnts/hr." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2280m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Greased and inspected casing tong" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1981m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Continued POOH with tubing from 2280 mMD to 1981 mMD. Average pulling speed 8 jnts/hr" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled out one additional joint and removed control lines in order to have slick joint through BOP while in slips. Meanwhile: Performed TBT for R/D csg handling equipment" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: R/D csg handling equipment" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed drops check on TDS." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U spear assy from set-back and stabbed into tubing" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior for engaging spear in tubing and tag TOC" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Engaged spear in 7' tubing" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 1971m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips" "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2764m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: RIH with tubing on 5 1/2' DP from 1971 mMD to 2764 mMD. Average running speed 528 m/hr." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2764m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Investigated fault on VFD failure on drawworks motor #3. De-assigned motor #3." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2853m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with tubing on 5 1/2' DP from 2764 mMD to 2853 mMD." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2880m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Established circulation 560 lpm / 13 bar and washed down to 2880 mMD. Set down 10 ton." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2894m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Stopped pumps. Unable to set down all tubing weight in order to release spear. Continued RIH from 2880 mMD to 2894 mMD. Set down all tubing weight, 60 ton. Released spear." "On 2016-07-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 780m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Dropped drift and POOH with spear assy from 900 mMD to 780 mMD." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 40m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued POOH with spear assy from 780 mMD to 40 mMD." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Retrieved drift. Pulled spear to surface and R/B same." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for retrieving surface MS-T seal assembly" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor. Removed PS-21 slips and installed master bushing." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U and function tested MS-T seal retrieval tool" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with MS-T seal retrieval tool. Landed out on energizing ring threads. Enganged retrieval tool." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressured up energizing lock ring line to 103 bar and bled off pressure in line. Released MS-T seal assembly" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS and pulled free seal assembly with 51 ton overpull. Retrieved MS-T seal to surface." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: B/O retrieval tool and L/O same" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared drill floor and removed casing tong" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT for cutting 10 3/4' tie-back casing" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U cutter/spear assembly" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH with cutter/spear assembly to 126 mMD" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Broke circulation. Staged up pumps to 500 lpm / 76 bar. Recorded up/down weight 74 / 71 ton." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Positioned cutter at 126 mMD and cut casing. Observed positive indications of cut." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Pumped out of hole with 280 lpm from 126 mMD to 21 mMD." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Attempted to engage spear several times, no positive indications of latch." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH to surface and discovered CH and tie-back casing was coming out with spear assy. Observed spear not properly latched. Attempted to release spear on surface." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Closed annular with 400 psi and lined up through choke. Attempted to release spear while rotating and pumping at 2000 lpm / 21 bar." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT and discussed way forward" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: R/U casing tong and elevator" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled out CH and 10 3/4' tie-back casing, total length 6,7m. Observed that adjustment sub had parted." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O cutter/spear assy with fish." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Discussed way forward. Meanwhile: Changed out elevator" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D casing tong" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: P/U Itco spear and re-configured BHA to fish 10 3/4' tie-back casing." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 30m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH and engaged spear. Up/down weight 72 / 69 ton." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with spear and fish. Secured 10 3/4' tie-back casing in rotary. Released spear and R/B same. Internal thread sleeve from adjustment sub stuck at grapple." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: R/U casing tong and changed dices to 11 3/4' for breaking out remaining slick part of adjustment sub. Attempted to break connection between casing pup and adjustment sub" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for using rig tongs to break connection between casing and adjustable sub" "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.5 hours. Operational details: Re-built dog collar to lift adjustable sub. Prepared rig tongs to break connection. Rig tongs not big enough to break connection on adjustable sub (11,5in). Meanwhile: Located bigger dies for casing tong and installed same. Broke connection between adjustable sub and casing with casing tong. L/O fish." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for pulling and L/O 10 3/4' tie-back casing." "On 2016-07-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.0 hours. Operational details: POOH with 10 3/4' tie-back casing from 100 mMD to surface." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for R/D casing tong" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: R/D casing equipment" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Changed handling equipment to 5 1/2'" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for M/U jet sub/torque tool BHA" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U jet sub/torque tool BHA" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 129m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH with jet sub/torque tool BHA from surface to 129 mMD. Took 6 ton weight. Unable to run torque tool into casing stump. Attempted to run into casing with and without rotation." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with BHA and L/O same" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Prepared 12 1/4' taper mill BHA" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT for M/U 12 1/4' Taper mill" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: P/U and M/U 12 1/4' Taper mill BHA" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP and tagged top of casing cut at 126,3 mMD." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' Taper mill - change of plans to avoid overtorqueing tie-back adapter during milling." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: L/D 12 1/4' Milling BHA" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Discussed situation with land organization Meanwhile: Prepared 9 1/2' Taper mill" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.0 hours. Operational details: Prepared plan for dressing off top of casing. P/U CH mill and B/O stab. M/U assy and L/O. Rearranged pipe in derrick to access over-torqued pipe in set-back." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Performed TBT for dressing off top of cut. Meanwhile: Performed drops check on TDS." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 43m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.0 hours. Operational details: P/U and M/U 9 1/2' Taper mill BHA" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: RIH with milling BHA from 43 mMD to 120 mMD." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Filled pipe and established circulation 200 lpm / 7 bar. Up/Down weight 78/74 ton. Tagged top of casing cut at 126 mMD with 5 ton." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.8 hours. Operational details: Rotated pipe 15-20 deg and passed restriction. Worked string up/down without flow and rotation several times. Max overpull 15 ton. Overpull decreased to 0 ton after working up/down repeatedly." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: Pulled above cut. Staged up pumps to 2000 lpm and initiated rotation 60 RPM. Free rot. torque 1 - 5 kNm. RIH slowly until torque increased. Increased rotation to 120 RPM. Milled off torque and continued RIH slowly until torque increased again. Repeated until entire Taper mill passed through top of cut w/o taking weight. Worked up/down with flow and rotation several times to polish cut." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 126m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT prior to POOH" "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: POOH with milling BHA." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Measured gauge on mill, 9 1/2'. Observed wear on upper part of Taper mill. L/D milling BHA." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Serviced and performed drops check on FWD PRS." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with jet sub/torque tool BHA." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U jet sub/torque tool BHA." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 143m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH with jet sub/torque tool BHA. Esablished circulation prior to entering cut, 120 lpm. Tagged no-go with 6 ton at 143m. Released tie-back adapter by rotating 6,5 turn LH. Released at 11,7 kNm." "On 2016-07-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with jet sub/torque tool BHA" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued L/D jet sub/torque tool BHA. Cleaned and cleared drill floor. Meanwhile: Prepared to run spear BHA" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with spear to fish casing stump and tie-back adapter." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U spear assy and set in slips. Removed thread sleeve from adjustable sub (left on the grapple from previous fishing run)." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH w/spear to 130 mMD. Engaged spear inside casing stump." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH w/spear and fish. Observed 2 ton overpull. Secured fish in slips and released spear." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/O fish" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O fish and R/B spear" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor. Meanwhile: Prepared equiment to run guns." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for handling guns" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: P/U and M/U gun BHA" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: RIH w/guns to 145,3 mMD" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Confirmed line up and closed BOP. B/O TDS and dropped ball. M/U TDS and started pumping with low rate. Guns fired at 139 bar. Continued circulating with 900 lpm / 6 bar. Lost 8m3 after firing guns." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Circulated B/U through choke. Max 1% gas measured on mud logging gas trap. No H2S detected." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Flow checked well for 5min through fully open choke, static. Opened BOP and flow checked well on TT for 10min, static." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: POOH to surface" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: L/D perforation BHA" "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT for M/U casing hanger mill." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.5 hours. Operational details: P/U taper mill assy and removed stab and DC from taper mill run. P/U casing hanger mill and M/U same." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: P/U and M/U 8 1/4' DC. RIH w/ milling BHA to 135m." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: M/U TDS and RIH from 135mMD to 141 mMD. Established parameters 2000lpm/15bar, 80RPM/1-4kNm. Up/down weight 87/84ton. Tagged CH with 2 ton at 141,29 mMD." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 6.2 hours. Operational details: Milled 10 3/4' CH from 141,29mMD to 141,45mMD. Stalled out several times. Tried different parameters to maximize progress. Parameters: 1000-2000lpm/4-15bar, 60-120RPM/4-25kNm, avg ROP 2,6cm/hr." "On 2016-07-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 5.0 hours. Operational details: Continued milling 10 3/4' CH from 141,45mMD to 141,51mMD. 2000 lpm/15 bar, 80-120rpm/4-25kNm, 3-6ton WOB, ROP 1 cm/hr. Experienced vibrations and string stalling out several times. Attempted to manipulate parameters to increase ROP." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.0 hours. Operational details: Continued milling 10 3/4' CH from 141,51mMD to 141,58mMD. 2000 lpm/15 bar, 80-120rpm/4-25kNm, 3-6ton WOB, ROP 2,3 cm/hr. Observed 170ltrs gain, max 3ppm H2S in fluid and a small gas peak at 141,54mMD, indicating that casing parted from CH. Experienced vibrations and string stalling out several times." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Picked up mill above CH. Stopped rotation and slided down through CH. Took weight at depth where milling was stopped." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Continued milling from 141,58 mMD to 141,66 mMD (~10cm past mark on DP). Stalled out several times and experienced vibrations at surface." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Attempted to slide through CH. Took weight at depth where milling was stopped." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Lined over to TT and performed TBT for drops check after severe vibrations." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Lined over to TT. Performed drops check of TDS and in BOP area." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Circulated 2 x B/U at 3000 lpm / 30 bar. 1,5kg swarf on ditch magnets on flowline." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 35m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: POOH with milling BHA" "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 35m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT for L/D milling BHA" "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: B/O XO, L/D 8 1/4' DC single and R/B 2 ea std 8 1/4' DC." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 36m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: P/U and M/U 12 1/4' flat bottom mill and RIH to 36 mMD." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 36m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Checked TDS after milling operation. Found hydraulic leak and repaired same." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: RIH with flat bottom mill from 36 mMD to 135 mMD" "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Established circulation and recorded up/down weight 86/83 ton. Established parameters 80 rpm / 1-4 kNm, 2000 lpm / 15 bar. RIH and tagged top of hanger at 139,7 mMD." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.0 hours. Operational details: Worked through CH. 40 - 140 RPM / 3 - 30kNm, 2000 lpm / 15 bar. Worked down 40 cm. Experienced vibrations at surface. String stalled out several times." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Tagged top of casing at 141,7 mMD (~1,5m below CH). Dressed off 10cm from top of casing. 100 RPM / 3-8 kNm, 2000 lpm / 14 bar." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Circulated 1 x B/U at 3500 lpm / 40 bar." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: POOH 1 std. Attmpted to break out TDS. Broke between upper and lower IBOP. Used work basket to assess situation and performed drops check. Spun in main shaft to lower IBOP. Lowered string and set in slips." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for changing saver sub" "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'interruption -- repair' and lasted for 2.8 hours. Operational details: Changed saver sub and M/U to lower IBOP." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Performed TBT for changing saver sub with new ongoing crew Meanwhile: Prepared new saver sub." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: Spun in shaft to IBOP, lifted pipe handler into position and M\U saver sub to IBOP 88kNm M/U torque ring and installed lock-ring." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed drops check on TDS." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Adjusted pipe handler on TDS." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT for POOH with milling BHA" "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 101m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: POOH 1 std and R/B. L/O pup joint" "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Continued to POOH. Unable to B/O Xover on 8 1/4 DC due to over-torque, max 160kNm. Changed out dies on IRN and attempted to B/O. M/U lift-sub and R/B DC with XO installed." "On 2016-07-19, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: POOH w/ BHA to 27 mMD, R/B 8 1/4' DC." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 27m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Continued POOH to surface" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.0 hours. Operational details: L/D BHA. Experienced over-torqued connection. Needed to clean jaws on IRN and break connections with 160 kNm. Cleaned and cleared drill floor" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT for M/U and RIH with cutter BHA" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 17m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: P/U and M/U cutter BHA. P/U and M/U 1 std 5 1/2' DP." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 17m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Installed PS-21 slips in rotary table." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 701m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from 17 m to 701 m . Avg. tripping speed 390 m/hr." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 701m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Pulled out PS-21 slips and installed masterbushing" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 701m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT for P/U and M/U spear assy" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 701m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: P/U spear assy from derrick and stroke out bumper sub. B/O bullnose at bottom." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 711m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: Installed XO and M/U spear assy" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 827m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from 711 m to 817 m . Avg. tripping speed 230 m/hr." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 853m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Filled pipe. M/U TDS and recorded up/down weight 100/95 ton. Continued RIH to cutting depth at 853 mMD. Engaged spear. Initiated circulation 1675 lpm / 78 bar and cut 10 3/4' x 9 5/8' casing at 850 mMD. Lost 40 ton weight. Up weight with fish 155 ton. Released spear." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 748m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH w/ cutter BHA on 5 1/2' DP from 853 m to 748 m." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 760m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: Observed 0,4 m3 gain in trip tank. Spaced out and closed annular preventer. Monitored choke pressure for pressure build up - no pressure build up observed. Circulated over choke 200 lpm for 30 min. Monitored choke for pressure build up. Opened BOP and flowcheck 15 min - slight gain in Trip tank." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 760m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Function tested BOP" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 760m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Investigated slight gain in trip tank. Found fresh water leaking into flowline." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 706m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: Continued POOH w/ cutter BHA on 5 1/2' DP from 760 m to 706 m. Inspected spear assy and R/B same. L/O XO." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 706m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 17m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH w/ cutter BHA on 5 1/2' DP from 706 m to 17 m . Avg. tripping speed 680 m/hr." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 17m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed master bushing" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: L/D cutter BHA." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cleaned and cleared drill floor." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for P/U and M/U spear BHA" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U spear BHA" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 154m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH w/ spear BHA to 154 m and tagged top of casing. Enganged spear." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH w/ spear BHA and fish on 5 1/2' DP." "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled master bushing Installed 10 3/4' casing slips" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for R/U casing equipment" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled perforated casing pup and set in slips. Released spear and R/B" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 706m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/U handling equipment for pulling casing" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 706m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for L/O perforated casing pup joint" "On 2016-07-20, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 706m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: L/O perforated casing pup joint. R/U pipe washer in rotary." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 691m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: L/O first casing joint" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 691m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: R/U power roller system" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 670m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: POOH with 4 casing joints using clepo protectors. No practical way of using clepo, started to use regular pin protectors" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 383m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.5 hours. Operational details: POOH with 10 3/4' csg from 670 m to 383 m . Average 8,8 joints/hr." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 383m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Observed gain in TT. Closed Annular preventer and installed FOSV. No pressure in well. Investigated gain." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 383m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Opened BOP and monitored well on trip tank, static." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 383m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Removed FOSV and pulled 1 joint and removed slips to look into rotary table. Continued investigation." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 383m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: RIH, closed annular and installed FOSV. Monitored pressure in well, 0 bar. Continued troubleshooting." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 383m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: Continued investigation of TT gain / drains on rig floor. Found 6' drain line blocked and diverted through a 2' line to rig's drain system. 2' line too small to handle heavy rain, causing overflood in the diverter which again caused gain in TT. Opened annular preventer and monitored well on TT. Meanwhile: performed maintenance on Drawworks." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 383m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT prior to continuing pulling casing" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 246m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: POOH with10 3/4' x 9 5/8' casing from 383 m to 246 m. Average 11 joints/hr." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 246m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Changed to 9 5/8' handling equipment" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.0 hours. Operational details: POOH with 9 5/8' casing from 246 m to surface. Average 10 joints/hr." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for R/D casing equipment" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: R/D handling equipment" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT for M/U cutter BHA" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U and M/U 13 3/8' cutter assy to 5 1/2' DP" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from surface to 140 m. Unable to pass casing hanger with 12 1/4' Taper mill" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: M/U TDS. Attempted to work past restriction 20 rpm / 5kNm." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: POOH w/ cutter BHA to surface" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Removed slips and installed master bushing. Inspected and gauged mill and stab. Taper mill gauged slightly bigger than 12 1/4'. B/O and L/D 12 1/4' taper mill and 12 1/4' stab" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with new BHA" "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: M/U new cutter BHA with 12' taper mill and 12' string stab." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from surface to 140 m. No restrictions observed through CH. Removed master bushing and installed PS-21 slips." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 841m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from 140 m to 841 m. Avg RIH speed 700 m/hr." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 841m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: M/U TDS, filled pipe, 400lpm/33bar. Trapped 25 bar behind IBOP and recorded free rot. torque at 100 rpm / 4 kNm." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 841m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cut 13 3/8' casing at 839 mMD, 80-100 rpm | 400 lpm / 37 bar. SPP dropped, positive indication of cut." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 841m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Flowchecked well, 200ltr gain over 15 min due to open valve from pit 10 to TT. Closed valve. Flowchecked well for 10 min, static." "On 2016-07-21, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 841m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Established circulation 300 lpm. RIH slowly and tagged cut at 839 mMD. 70 cm window length." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 841m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT prior to POOH" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: POOH w/ cutter BHA on 5 1/2' DP from 841 m to 40 m. Pulled wet. Avg. tripping speed 400 m/hr." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min prior to pulling BHA through BOP. Meanwhile: Removed PS-21 slips and installed master bushing" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: POOH to surface" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D cutter BHA" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: P/U and M/U the 13 3/8' EZSV plug BHA" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 820m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: RIH w/ 13 3/8' EZSV on 5 1/2' DP from surface to 820 m . Avg. tripping speed 370 m/hr." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 820m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS and filled pipe" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 830m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Established circulation and washed the setting area from 830 mMD to 825 mMD. Measured 5ppm H2S in gas trap. Installed the 13 3/8' EZSV plug at 827 m." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 807m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Disconnected TDS and dropped 3 1/5' drift with tail" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 42m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 807 m to 42 m. Avg. tripping speed 1000 m/hr." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 42m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Retrieved drift. Removed PS-21 slips and installed master bushing." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: L/D the 13 3/8' EZSV plug RT." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing EZSV plug." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.0 hours. Operational details: Attempted to pressure test 13 3/8' EZSV plug to 40bar/10min. Volume pumped higher than estimated. Estmiated volume to pressure up from 10 to 40 bar ~100 ltr. Investigated for surface leakage, no findings." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to RIH and pressure test EZSV plug from below." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: P/U and M/U 13 3/8' EZSV RT to 5 1/2' HWDP Removed masterbushing and installed PS-21 slips." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 78m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: RIH from surface to 78 mMD on 5 1/2' HWDP. Re-arranged pipe in derrick to reach last HWDP." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 827m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: RIH w/ EZSV RT on 5 1/2' DP from 78 m to 827 m. Avg tripping speed 600m/hr." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 827m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Stung into the EZSV plug, set down 10 ton. Performed TBT for pressure testing 13 3/8' EZSV from below." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 827m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Closed annular and pressure tested EZSV plug from below to 14 bar. Volume pumped 1100 ltr, bled back 900 ltr. Observed pressure increaseing on choke gauge. Opened annular and released RT." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 681m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 827 m to 681 m. VFD fault on FWD PRS." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 681m. The activity was categorized as 'interruption -- other' and lasted for 4.2 hours. Operational details: Troubleshoot and started repairing FWD PRS." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 681m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Continued troubleshooting and repairing FWD PRS" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 116m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Continued POOH w/ EZSv RT on 5 1/2' DP from 681 m to 116 m . Avg. tripping speed 750 m/hr." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 116m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Flowchecked well, static. Meanwhile: Removed PS-21 slips and installed masterbushing." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH with EZSV RT on 5 1/2' HWDP from 116 mMD to surface." "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U lift sub and pulled EZSV RT to surface. B/O and L/D XO for next run. L/D RT" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for M/U new cutter BHA" "On 2016-07-22, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: P/U old cutter assy, B/O and L/D float sub. L/D cutter assy. P/U new cutter assy and M/U to string magnet and XO. M/U float sub and XO." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: M/U TDS and tested new cutter at surface. Disconnected TDS" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 820m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from surface to 820 m. Avg. tripping speed 470 m/hr. Avg." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 820m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Filled pipe 800 lpm. Reduced rate to 200lpm when pipe was full" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 820m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Recorded parameters 600lpm / 68 bar, 400 lpm / 35 bar. Took up/down weight 95/90 ton. 1-6 kNm free rot. torque. Cut casing at 820 mMD, 80 rpm / 600 lpm. Saw pressure drop, indiaction of cut. Max torque when cutting 17 kNm." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 820m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Flowchecked well for 10 min, static." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 820m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Measured cut window, 80cm." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Disconnected TDS and POOH on 5 1/2' DP. Avg. tripping speed 510 m/hr." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Removed PS-21 slips and installed master bushing L/D cutter BHA. String magnet covered in swarf." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Cleaned and cleared drill floor." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for honing CH area" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 67m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: P/U and M/U milling BHA" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 135m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH w/ milling BHA from surface to 135m." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 135m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Filled pipe and recorded parameters, 80 rpm/1-4 kNm, up/down weight 80/77 ton, 2000 lpm/9bar. RIH and tagget obstuction at 141,5m with 1 ton." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 177m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Honed obstruction in CH area, 100 rpm/2-20 kNm, 2000 lpm/9bar. RIH with 12 1/4' stab below CH." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 177m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for POOH" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 67m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: POOH w/ milling BHA" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: L/D milling BHA" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Prepared for clean-out run. Cleaned and cleared drill floor." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for M/U and RIH with clean-out BHA" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 67m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: M/U clean-out BHA" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 67m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 806m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: RIH w/ clean-out BHA from 67 mMD to 806 mMD. Avg. running speed 740 m/hr." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 815m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Filled pipe and staged up pumps to 3100 lpm/36 bar. OBM in returns, got a gas peak of 18% and 8ppm H2S in return fluid. Staged up pumps to 4000lpm / 58 bar Made 4 passes with flow and rotation between 806 mMD and 815 mMD. 4000 lpm / 58 bar, 100 rpm/1-10 kNm." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 815m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pumped 10m3 hi-vis pill and circulated 1 x B/U." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 815m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Flowchecked well for 10min, static." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 81m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: POOH w/ clean-out BHA from 815 mMD to 81 mMD" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 81m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Flowchecked well, static. Meanwhile: Removed PS-21 slips and installed masterbushing" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: L/D clean-out BHA. Cleaned and cleared drill floor." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for M/U new 13 3/8' EZSV plug and RT" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: P/U and M/U running tool and 13 3/8' EZSV plug" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH w/ 13 3/8' EZSV BHA slowly until below CH. No obstructions seen." "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips" "On 2016-07-23, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 728m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: RIH restricted w/ 13 3/8' EZSV BHA to 728 mMD, 2 min/std." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 808m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Continued RIH restricted with 13 3/8' EZSV plug BHA to 808 mMD. 2 min/std." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 808m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Established circulation and washed the setting area between 808 mMD and 815 mMD, 800 l/min. Set EZSV plug at 811 mMD." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 770m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Racked back one stand. M/U TDS and spaced out to close UPR. Meanwhile: Prepared cement unit for pressure testing." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 770m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Flushed lines, confirmed line-up and performed line-up test to 40 bar. Meanwhile: Performed drops check and serviced TDS." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 770m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Closed UPR and attempted to pressure test EZSV plug from above to 40 bar. Stopped pumping at 30 bar. Volume pumped not according to theoretical volume. Estimated volume ~100ltr from 10 to 40 bar. Trip tank stable. Volume pumped 600 ltr, bled back 400 ltr. Meanwhile: Serviced TDS" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Disconnected TDS and stung into EZSV plug. Tagged plug at 811 mMD, sat down 9 ton." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Closed UPR, lined up to pressure down drillpipe. Pressure tested EZSV plug from below to 14 bar. Observed pressure increase on choke gauge to 14 bar. Trip tank stable. Volume pumped 650 ltr, bled back 650 ltr." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Evaluated situation. Decided to POOH. Meanwhile: Bled down pressure on cement unit and released EZSV RT" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for POOH" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 770m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Stung out of EZSV plug and disconnected TDS. R/B 1 std." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 40m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: POOH from 770 mMD to 40 mMD. Avg tripping speed 730 m/hr" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed PS-21 slips and installed master bushing R/B last stand" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: L/D EZSV RT BHA." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for slip and cut drill line." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Hung off block" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Emergency training - handling gas/H2S on rig floor, shakers and pump room." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Slip and cut drill line" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 6.8 hours. Operational details: Troubleshoot issue with stuck lock pin on dead line anchor. Replaced sheared off pins on dead line anchor motor. Removed stuck lock pin. Assembled motor." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued slip and cut. Removed hang-off wire" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Calibrated drawworks" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with RTTS plug" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 88m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: P/U and M/U 3 std 8 1/4' DC to RTTS assy." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 88m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed handover meeting with new drilling crew" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 88m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: P/U and M/U storm valve" "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 130m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH with RTTS BHA restricted to 130mMD, 2 min/std." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 160m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: RIH to plug setting depth and washed setting area, 600 lpm / 2bar Set RTTS plug at 161 mMD." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 161m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Lined up cement unit to standpipe and confirmed line-up. Attempted to test lines against IBOP to 40 bar. Closed stand pipe valve and got acceptable line test." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 161m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Pressure tested between RTTS plug and EZSV plug at 811 mMD to 40bar/10min. Volume pumped from 10 to 40 bar 143 ltr, bled back same." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 98m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Released RTTS plug and POOH restritcted from 161 mDM to 98 mMD, 2 min/std." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: L/D RTTS and RT. R/B 8 1/4' DC." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for RIH and punching 13 3/8' casing. Observed hydraulic leak from PRS." "On 2016-07-24, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Investigated and started to repair hydraulic leak on AFT PRS. Meanwhile: Cleaned deck for hydraulic oil." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 7.0 hours. Operational details: Continued repairing leakage on AFT PRS. Meanwhile: Started to repair FWD PRS" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 8.2 hours. Operational details: Continued repairing both PRS's. Function tested AFT PRS and confirmed no leakages. Pulled electrical cable through drag chain on FWD PRS. Meanwhile: Performed drops inspection on AFT PRS." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for handling guns and perforating 13 3/8' casing below CH" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 25m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: M/U perforation guns" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: RIH restricted w/ guns to 140 mMD, 2min/std." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 147m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: M/U TDS and spaced out to have top gun at 143,3mMD. Closed UPR and confirmed line-up. Flushed ball seat area." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 147m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Dropped ball. M/U pup joint and spaced out. Closed UPR and pressured up to 140 bar. Got positivie indications of fired guns, lost all pressure. Top shot at 143,3 mMD, btm shot at 146,3 mMD." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 147m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Circulated at 450 lpm until returns. Staged up flow to 1000 lpm / 5 bar. Circulated 1 x B/U, no gas observed, 5ppm H2S in gas trap after pumps was stopped." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 147m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Flowchecked well through choke, static." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 147m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Opened BOP and lined up to TT. Flowchecked well, static." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 26m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: POOH with guns from 147 mDM to 26 mMD." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: L/D 1 5 1/2' DP single and perforation BHA" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor Meanwhile: Prepared to RIH with EZSV RT" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with EZSV RT" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 2m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U and M/U EZSV RT" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: RIH w/ EZSV RT on 5 1/2' DP from 2 mMD to 364 mMD . Avg. tripping speed 344 m/hr." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed master bushing and installed PS-21 slips" "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 767m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: RIH w/ EZSV RT on 5 1/2' DP from 346 mMD to 767 mMD. Avg. tripping speed 560 m/hr." "On 2016-07-25, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 767m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed 2 x pups and pump in sub. M/U pump-in sub and L/D pump-in stand." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 767m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Continued M/U pump-in stand." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 807m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Continued RIH from 767 mMD to 807 mMD." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 811m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U pump-in stand. M/U TDS, took up/down weight 94/88 ton. Washed top of EZSV 1000 lpm / 5 bar. Stung into EZSV plug at 811 mMD. Sat down 10 ton." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 811m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.2 hours. Operational details: Closed UPR and lined-up for displacing annulus to SW. Pumped 20m3 hi-vis pill followed by SW. Max gas peak 5%, max H2S peak 4ppm in gas trap, no H2S measured in air. Stopped pumping when clean SW in returns and gas readings decreased below 2%, totally pumped 140m3 SW. Meanwhile: Performed TBT for cement job. Tested dump line." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 811m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Opened BOP. Lined up to TT and flowchecked well for 10 min, static." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed cement hose. Meanwhile: Prepared to pump wash pill." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Pumped 20 m3 of wash pill, 1200 l/min/ 13 bar. Mixed and pumped 35 m3 of 1,95 SG cement slurry, 580 lpm / 15 bar. Full returns. Displaced cement down drill string with 11 m3 FW at 1200 lpm. Pressure increased from 17 bar to 61 bar during displacement." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Stung out of EZSV plug and picked up 2,5 m above the plug. Mixed and pumped 7,7 m3 1,95 SG cement slurry, 600 lpm / 15 bar. Displaced cement with 7 m3 FW, using cement pump, 1000 lpm / 15 bar." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed cement hose and L/O cement stand." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 700m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: POOH 2 stands to 700 mMD. Installed sponge ball. Circulated 1 x B/U, 3500 lpm/ 32 bar at 50 rpm. Max gas 9%, 5 ppm H2S in gas trap at B/U. No H2S measured in air. Dumped returns when clean SW at shakers." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 80m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Disconnected TDS. POOH w/ EZSV RT on 5 1/2' DP from 700 mMD to 80 mMD. Avg. tripping speed 620 m/hr." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 80m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed master bushing" "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH from 80 mMD to surface, using manual slips." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed springs from EZSV RT, B/O and L/D same. P/U cement stand. B/O and L/D 2 pup joints and pump-in sub." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: WOC Meanwhile: P/U Wellbore fishing assembly. B/O and L/O XO and jetting sub." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: WOC Meanwhile: Function tested shear ram. RIH with jetting sub, spaced out and function tested all BOP rams. M/U to TDS and jetted BOP 3 x passes. POOH with jet sub." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.8 hours. Operational details: WOC Meanwhile: Isolated drilling equipment and performed maintenance. Pressure tested AFT PRS Hyd hoses. Performed PMs and inspections on FWD PRS Performed PMs on TDS traveling equipment Prepared equipment for changing out PRS wires." "On 2016-07-26, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.0 hours. Operational details: WOC Meanwhile: Continued performing rig maintenance. Performed PMs and inspections on FWD PRS. Performed PMs on foxhole. Megger tested TDS from switch board room. Removed pop off on stand pipe manifold and pressure tested stand pipe drag chain hoses to 520 bar. Prepared for N/D diverter and BOP" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Continued performing rig maintenance." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing cement plug. Meanwhile: Checked line-up and flushed lines." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Checked bucket sample. Sample indicated set cement. Closed BRS and attempted to pressure test cement plug to 125 bar. Pressure reached 45 bar and broke off. Stopped pumping, pressure continued to drop. Bled off pressure to cement unit. Volume pumped from 10 to 45 bar 330 ltrs. Bled back to 10 bar, 280 ltr. No increase in trip tank. Checked for surface leaks." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: WOC for 2 hours. Meanwhile: Performed drops inspection on FWD PRS and performed PMs." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Verified line-up and attempted to pressure test cement plug to 125 bar. Pressured up to 10 bar reference pressure and stopped pumping. Pressure dropped back to 2 bar. No increase in trip tank." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Prepared to run RTTS. Measured 8 1/4' DC joints and verified RTTS measurements. Opened BSR and observed 600ltr instant loss on TT followed by stable lossrate of 1,08 m3/hr." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 26m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: P/U 3 singles 8 1/4' DC from cantilever and RIH to 26 mMD. Loss rate 1,08 m3/hr" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 80m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: P/U and M/U 3 stands 8 1/4' DC from set-back and RIH from 26 mMD to 80 mMD. Loss rate 1,08 m3/hr" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 98m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: P/U and M/U the RTTS plug and storm valve. RIH to 98 mMD. Loss rate 1,08 m3/hr" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 218m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH w/ RTTS plug on 5 1/2' DP from 98 mMD to 218 mMD. Loss rate 1,08 m3/hr" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 218m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: M/D TDS and took up/down weight 92/87 ton. Loss rate 1,08m3/hr" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 226m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH from 218 mMD to 226 mMD and set plug above perforations on 13 3/8' csg and below 13 3/8' CH, mid packer element at 141,7mMD. Set down 19 ton on plug. Losses stopped. Monitored well on TT." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 226m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Evaluated situation with onshore organisation. Meanwhile: Monitored well on TT. Performed PMs." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 226m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Lined up to drill string. Confirmed line-up. Attempted to pressure test cement inside 13 3/8' csg and cement in annulus between 20' and 13 3/8' csg. Pressured up below RTTS plug to 20 bar and stopped pumping. Pressure started to bleed off immedietly. Trip tank stable. Pumped 620 ltrs and bled back 130 ltrs from 10 to 20 bar. Closed IBOP and pressure tested lines to 20 bar, no surface leakages observed." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 236m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Lined up down kill line. Closed BOP and pressure tested RTTS plug, production riser, tie-back connector, WH and CH. Pressured up above RTTS to 50 bar/10min. Pumped 30 ltr from 10 to 50 bar. Bled back same." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 236m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Released RTTS plug, 92 ton up weight. Waited 3 minutes for rubber elements to retract. RIH and set RTTS plug below perforations in 13 3/8' csg at 150 mMD (mid packer element). Sat down 16 ton. Loss rate 1,2 m3/hr." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 236m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Pressure tested cement inside 13 3/8' casing. Pressured up below RTTS to 50bar/10min, OK. Pumped 10 ltrs from 10 bar to 50 bar, bled back same. Losses on TT, 1,2 m3/hr." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 236m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Released RTTS plug. Waited 3 minutes for rubber elements to retract." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 98m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH w/ RTTS plug and storm valve on 5 1/2' DP from 236 mMD to 98 mMD." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 98m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: B/O storm valve. Inspected RTTS and storm valve. M/U storm valve to RTTS plug. Loss rate 1,2 m3/hr" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 226m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH w/ RTTS plug on 5 1/2' DP from 98 mMD to 226 mMD." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 226m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Set RTTS plug at 141,7 mMD (above perforations in 13 3/8' csg) w/ 4 stnd 8 1/4' DC below. Losses stopped. Backed out from storm valve, 18 turns LH. Top storm valve at 134,34 mMD." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH with RTTS RT to surface." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Closed BSR and pressure tested RTTS plug, production riser, tie-back connector, WH and CH. Pressured up above RTTS to 50bar/10min. Volume pumped 30 ltr, bled back same." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: R/B RTTS RT." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/D BOP and surface riser." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed elevator and installed 25T chains to TDS bails." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled master bushing and installed pad eyes in rotary. Attached chains to pad eyes" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Observed 80 bar on B-annulus gauge. Investigated issue, faulty gauge. Opened B-annulus valve. Observed fluid running out due to utubing." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Drained surface riser. Adjusted BOP tensioners and carrier. Bled off diverter over-shot." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Disconnected tensioner pistons. Meanwhile: Prepared to pull diverter." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling diverter" "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued disconnecting cylinders and cleaned up tools in the area." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Pulled diverter and R/B in set back. Pulled slick joint and L/O same." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/D surface HP riser." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Disconnected NT2 connector on surface HP riser. Cleaned and inspected stump." "On 2016-07-27, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for moving BOP" "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Skidded BOP from well center to test stump." "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed scaffolding in moonpool" "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for removing hatches" "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Rigged up lifting equipment and removed hatch covers and split hatches from F-15." "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling surface HP riser" "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Rigged up lifting arrangement with double securing. Disconnected surface HP riser from multibowl and pulled riser to drill floor." "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed master bushing" "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/D surface HP riser. Cleaned seal face and protected same." "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed hatches on F-15 and prepared to skid over to F-7." "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U NT2 connector on test stump and removed scaffolding. Removed bridge from production unit to cantilever. Cleaned and cleared moonpool" "On 2016-07-28, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Continued removing scaffolding in moonpool. Meanwhlie: Pulled cement hoses from wellhead to moonpool. Loosened bolts on F-7 hatch. ************** End of reporting *******************" "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Completed pre-skid checks. Prepared to skid cantilever" "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding cantilever" "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded cantilever to F-15 D." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Removed hatch on F-15. Installed halfmoon hatch. Checked alignment." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed hi-pressure riser and M/U connector on WH." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Built scaffolding in moonpool." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Moved BOP to well center. Landed same on HP riser." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/U BOP with ongoing crew" "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: N/U BOP. Meanwhile: Prepared tension cylinders. Installed tension cylinders." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed slipjoint." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed diverter" "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U slipjoint to BOP. Meanwhile: Filled well from trip tank. R/D chains and installed BX elevator and rotator." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for connector test Meanwhile: Lined up to cement unit." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed connector test to 20/115 bar for 5/10 min." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for P/U and RIH with RTTS RT" "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 4m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: P/U and M/U the RTTS RT BHA. Checked and greased tool." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ RTTS RT on 5 1/2' DP from surface to 130 m." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: M/U TDS and pumped 150 lpm / 5 bar. Recorded up/down weight 71/68 ton, set down 1 ton on RTTS Rotate 22 turns. No pressure observed below RTTS." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Released RTTS packer. Waited 10 min for packer elements to retract. Observed trip tank slowly decreasing, then leveling out." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flowchecked well, 90 ltr loss over 15 min." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH w/ RTTS packer on 5 1/2' DP from 130 m to surface." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: L/D storm valve, RTTS RT and packer." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: L/D 4 stands 8 1/4' DC, high torque needed to break connection, 130kNm." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor. Meanwhile: Performed TBT for pressure testing OH to surface cement plug" "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Attempted to pressure test OH to surface cement plug to 115 bar, pressure bled off after reaching 10 bar. Static losses 1,2 m3/hr." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT for cutting 13 3/8' casing." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U and M/U 13 3/8' cutter BHA." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 53m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH w/ 13 3/8' cutter BHA on 5 1/2' DP from surface to 53 m." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 53m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Installed PS-21 slips." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 694m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Continued RIH w/ cutter BHA on 5 1/2' DP from 53 m to 694 m. Avg. tripping speed 640 m/hr." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 700m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Established paramters. Up/down weight 92/87 ton. 400 lpm / 34 bar, 500 lpm / 57 bar, 600 lpm / 76 bar. Positioned cutter at 700 mMD. Cut 13 3/8' casing, 600 lpm / 57 bar, 80 rpm. Pressure dropped, good indication of cut. Observed H2S gas at shaker, 11 ppm H2S in air, 52ppm in gas trap." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 700m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.2 hours. Operational details: Circulated 500 lpm / 52 bar through mud/gas separator due to H2S. Circulated until H2S out of well, pumped totally 72 m3. Treated return pits with H2S scavenger." "On 2016-09-15, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 453m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: POOH w/ cutter BHA on 5 1/2' DP from 700 m to 453 m. Avg. tripping speed 330 m/hr." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 453m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Reset PRS electronics." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Continued POOH w/ cutter BHA on 5 1/2' DP from 453 m surface . Avg. tripping speed 600 m/hr." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Changed handling equipment" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D pup joint. Inspected cutters, and taper mill. L/D cutter assy." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor. Static losses 0,5 m3/hr over 10 min." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: P/U and M/U the 13 3/8' EZSV plug BHA. Installed springs on centralizer." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed PS-21 slips" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH w/ EZSV plug BHA on 5 1/2' DP from 0 m to 30 m. Hung up on restriction at 30m. Re-attempted to run past restriction, same HUD." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Pulled BHA to surface and inspected tool. Found cement in holes for springs on centralizer, which possibly interrupted spring movement. B/O and L/D EZSV RT, P/U backup, found cement on backup RT. Cleaned off cement. M/U BHA." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 42m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH slowly w/ EZSV plug BHA from surface to 42 m. Passed restriction at 30m." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 42m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Installed PS-21 slips." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 285m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH w/ EZSV plug BHA on 5 1/2' DP from 42 m to 285 m. Restricted running speed 2 min/std. Observed hydraulic leak on IRN." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 285m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Repaired hydraulic leak IRN." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 695m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Continued RIH w/ EZSV plug from 285m to 695m" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 695m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Washed setting area from 695m to 685m w/ 800 l/min - 6 bar" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Set EZSV at 690m bottom plug. Sheared at 27T and tagged w/ 5t. Released stinger with 22 turns" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed master bushing" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/B stand, P/U and M/U 3m pup and cement stand for space out" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Stang back into EZSV and M/U cement hose" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Verified line up and performed integrity test to 100 bar between FOSVs on cement assy" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Attempted to pressure test below EZSV to 20 bar, meanwhile monitored trip tank, observed 500 l/min losses. Failed test" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Closed UPR and lined up to monitor annulus through choke. Pressured up annulus through kill line to 35 bar whilst monitoring below EZSV with 5 bar at the cement unit through cement assy. Observed no pressure build up on the drill pipe side. Confirmed hydraulic isolation of annulus cement plug" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 10m3 wash pill at 2500 l/min - 19 bar" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Balanced cement plug (590 m - 690 m ): Mixed and pumped 7,8 m3 of 1,95 SG cement slurry, 600 l/min. Displaced the cement with 7,2 m3 of drill water. TOC 590 m." "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Broke off cement hose and 3m pup w/ cement assy, L/D same" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 500m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH with 5,5in DP from 687m to 500m w/ 2 min/stand. Flowback observed from 566m to 500m. M/U TDS and monitored pressure - 1 bar on standpipe gauge" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 500m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed sponge ball in saver sub and M/U TDS. Circulated 2x BU at 3500 l/min - 31 Bar" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 405m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH from 500m to 405m" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 405m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U Swaco washing tool from HTS with FOSV, M/U to string and stand of drill pipe from derrick" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 405m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Washed BOP, 3 passes, 1600 l/min - 14 Bar - 20 rpm - 1-4kNm" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 405m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Functioned BOP" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 405m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Washed BOP, 3 passes, 1600 l/min - 14 Bar - 20 rpm - 1-4kNm" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 405m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: R/B stand of 5,5in DP in derrick and L/D Swaco wash tool and FOSV, Drop 3in drift in string" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 405m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21 slips" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 16m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH from 405m to 16m" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 16m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed master bushing" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH from 16m to surface, removed spring centralizers, L/D EZSV running tool" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U diverter chains and bridle" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to N/D diverter and BOP" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: N/D diverter and BOP" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Took down scaffolding in moon pool" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lowered diverter chains through rotary and attached to HPDR" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed dogs on HPDR connector to well head" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled HPDR to rig floor and installed master bushing" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lowered rig floor tuggers down to moon pool hatches and prepared for removing the hatches" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to remove half moon cover and instal hatches in the moon pool. Meanwhile serviced drilling equipment" "On 2016-09-16, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Removed half moon cover, lather, hoses and installed hatches in the moonpool. Meanwhile worked through skidding check list REPORTING ON 15/9-F-1 C" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser Meanwhile: Performed TBT for skidding" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: Waited on weather to pull production riser Meanwhile: Skidded cantilever to F-15 D" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.2 hours. Operational details: Waited on weather to pull production riser Meanwhile: Removed hatch and hole covers. Performed TBT with ongoing crew Build scaffolding around hole openings" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Waited on weather to pull production riser Meanwhile: Installed scaffolding around hole openings in moonpool and WH Performed TBT for installing NT2 connector and P/U cutter BHA Cleaned shaker pits" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser Significant wave height 5,1m Meanwhile: Installed NT2 connector on Multibowl" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser Meanwhile: P/U Cutter BHA. Tested cutters on surface; Motor started at 100 lpm, knifes opened at 200 lpm." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: Waited on weather to pull production riser Meanwhile: RIH with cutter assy, 2 std 5 1/2' DP and Multibowl RT Engaged Multibowl RT in Multibowl." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: Circulated out top layer of fluid column in riser to drain, 150 lpm / 3 bar. Reduced rate due to overflow in drain system. Took fluid sample for analyzing." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.2 hours. Operational details: Waited on weather to pull production riser Removed riser tension system. Cleared rig floor for riser equipment from previous wells." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser Meanwhile: Performed TBT for displacing riser to clean SW" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather to pull production riser Meanwhile: R/U hoses from Multibowl to kill manifold in order to take returns to pit." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: Waited on weather to pull production riser Meanwhile: Removed boat collision stool Cleaned shakers and pits." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on weather to pull production riser Significant wave height reduced from 4,7m to 4m Meanwhile: Continued removing boat collision stool" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Attempted to displace riser to drain with 100 lpm / 3 bar. Leakage through Multibowl RT over the NT2 connector." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Increased flow rate to 1200 lpm / 60 bar. Less leakage. Displaced riser to clean SW." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D hoses from kill manifold." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Increased flow rate in steps to 2300 lpm / 80 bar. Cut production riser at 134,9 m. Significant wave height 3m" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for removing hoses and valve outlets on Multibowl." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D hoses and valve outlets from Multibowl" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling inner string" "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled Multibowl to drill floor. Disengaged Multibowl running tool and parked same in AFT PRS." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U false rotary and pulled inner string. R/B cutter BHA." "On 2016-10-17, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: R/D false rotary. Installed Multibowl RT. Removed C-plate. Pulled Multibowl and Tensioner joint, cleaned riser on centralizer deck. Installed master bushing and elevator. Landed Tensioner joint onto elevator." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: R/U cutting machine Cut Tensioner joint. Needed to change knifes due to jamming. Significant wave height between 2,4m and 2,8m R/D cutting machine" "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/O Tensioner joint and Multibowl." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U equipment for L/O Tensioner joint and Multibowl." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O Tensioner joint and Multibowl (Lift #1) Removed Multibowl RT and NT2 connector." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed handling tools and NT2 connector R/D elevator. Connected bails to manual elevator." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled upper pup and splash zone joint (Lift #2), cleaned riser on centralizer deck. Installed elevator on masterbushing and landed off riser." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 2,1m. R/D cutting machine" "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O splash zone joint (Lift #2)." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (Lift #3) Installed master bushing and elevator. Landed off riser onto elevator." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser joint. Significant wave height 1,6m. R/D cutting machine. Meanwhile: Performed TBT for L/O riser joint." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled riser (Lift #4). Cleaned off marine growth on centralizer deck. Installed master bushing and elevator. Landed riser onto elevator. Riser out of splash zone at 0800." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #4). Pulled riser (Lift #5). Cleaned off marine growth. Installed master bushing and elevator. Landed off riser onto elevator." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #5). Pulled riser (Lift #6). Cleaned off marine growth. Installed master bushing and elevator. Landed off riser onto elevator." "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine Meanwhile: Performed TBT for installing hatches" "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #6) L/O last joint (Lift #7)" "On 2016-10-18, at Well NO 15/9-F-15 D, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed hatches. Removed scaffolding **** END OF REPORT ****" "On 2009-04-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Removed hatch for F-10. Meanwhile :Ran foxhole and secured same." "On 2009-04-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Held toolbox meeting. M/U 36' BHA. Ran in and entered template at 142,4 m. Tagged seabed at 142,9 m." "On 2009-04-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Started to wash down at 600 - 1000 lpm, taking weight straight away. Started to rotate 20 RPM. worked pipe between 142,9 m - 144,7 m. Pulled back to 143,4 m and held 20 RPM and 1000 lpm. Stopped rotation and stopped pumps. ROV checked bit position." "On 2009-04-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 148m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled back down to 144,9 m. Stopped rotation and pumps. ROV moved into template to observe position of bit. Continued to drill, worked 26'/36' HO into slot. Drilled from 144,9 m to 148,1 m. 1000 lpm - 2300 lpm, 20 RPM." "On 2009-04-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 151m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Stopped rotation and pumps. ROV moved into template to observe position of centralizer drill bushing. Continued to drill from 148,1 m to 151 m. 1000 lpm, 20 RPM." "On 2009-04-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 36' hole from 151 m to 165 m. 80 RPM, 4 -5 ton WOB, 3000 lpm, trq 3 kNm, Took survey at 160 m. Inclination 0,28 deg. Pumped HIVIS pills as per program." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 207m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 36' hole from 165 m to 207 m (17 1/2' bit depth). 90-100 RPM, 5 ton WOB, 4000-4450 lpm, 3,7 kNm, ROP 5-20 m/hr. Pumped HIVIS pills as per program. Took survey at 170 m: Inclination 0,27 deg. Took survey at 180 m: Inclination 0,17 deg. Took survey at 190 m: Inclination 0,21 deg. Took survey at 206 m: Inclination 0,15 deg." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 207m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated 1,5 bottoms up with seawater. Pumped 40 m3 HIVIS pill at 4500 lpm. Displaced well to 1,40 sg WBM at 4500 lpm / SPP 128 bar, 10 RPM." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 167m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 36' BHA to 167 m." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 36' BHA to 147 m. Topped up hole with 1,40 sg WBM. POOH to 121 m." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH with 36' BHA to 36 m." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 36m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Investigated and repaired leak on AFT Iron roughneck." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 36' BHA to 8 m. Held Toolbox talk prior to remove bushings with low block height. Pulled Holeopener through rotary and laid out same." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Performed full derrick and top drive inspection." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held tool box talk- Rigged to run 30' conductor." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 1.0 hours. Operational details: Waited on crane / deck crew to unload boat." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held toolbox talk with deck crew and 3rd partys prior to pick up an run 30' Conductor. P/U and ran 30' Conductor shoe joint to 12 m. Filled shoe joint to check ball valve." "On 2009-04-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Held toolbox talk. P/U and ran 2 x 30' intermediate joints and 1 30' X-over joint. Changed out casing handling gear. Installed elevator rotator and M/U kevlar belt tongs. P/U 30' Conductor housing joint." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: M/U 30' Conductor housing joint. Ran carefully into splash zone with 30' Conductor. Waves and current was too high to continue operation and risk damaging adjacent production risers. Pulled up with 30' Conductor to above sea-level and double-secured same. Significant wave height 1,6 m. Max wave height 2,5 m." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: Waiting on weather to run 30' Conductor. Notified Maersk Production to bean up wells. While waiting on weather cleared rig floor. Removed frame and cage from HTS. Picked up cement stand. Started to pressure test BOP." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waiting on weather. Meanwhile pressure tested BOP to 1035 bar (15000 psi)." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waiting on weather. Meanwhile continued to make up cement stand." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waiting on weather. Meanwhile repaired leak on FWD PRS top jaw." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waiting on weather. Meanwhile calibrated FWD PRS. Lined up to test lower pipe ram (LPR) on BOP." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waiting on weather. Meanwhile rigged up and laid out MWD and 2 x 9 1/2' drill collars from derrick. Pressure tested LPR on BOP to 20 bar / 5 minutes and 1035 bar / 15 minutes. Prepared 26' BHA. Started to lay out 8 1/4' jar." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: Waiting on weather. Meanwhile held Toolbox talk with new crew. Continued to lay out 8 1/4' drill collars. Pressure tested stand pipe manifoil to 1035 bar (15000 psi). L/D 8 1/4' jar. Started to lift up last tension cylinder in moon pool." "On 2009-04-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waiting on weather. Meanwhile picked up 8 1/4' DC and racked in set back. Continued to install tension cylinder in moon pool." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waiting on weather. Meanwhile P/U 8 1/4' drill collars and racked back in set back. Installed last tension cylinder in moon pool." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waiting on weather. Meanwhile rearranged collar fingerboard to rack back BHA and lay out 6 1/2' jar." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waiting on weather. Meanwhile laid out 6 1/4' jar and 5' HWDP." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 45m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.8 hours. Operational details: Waited on weather. Issued notice to shut in adjacent wells at 06:45. Meanwhile removed end stops on HTS. Made up aluminium inner string on HTS." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed dog collar and pulled slips. Ran 30' conductor from 45 to 62 m MD." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed C-plate in rotary. Hung off conductor housing in C-plate. Removed CART handling tool. Filled conductor with SW." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Installed C-plate on top of 30' housing. Picked up and ran 2 ea premade lengths of aluminium stinger to 46 m inside 30' conductor. Made up x-over to pup below CART." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lowered CART and made up to 30' coductor housing with 5 counterclockwise turns. Installed inclinometer and valve handle on CART." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 65m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed C-plate from RT. Ran conductor housing through RT. Installed master bushing." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 30' conductor on 5 1/2' HWDP landing string from 65 m to 196 m MD. Marked pipe at 112,9 m to obtain relative distance top of conductor housing to Centralizer deck. Observed with ROV when comming through template." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Laid out 5 1/2' HWDP single. Made up cementing single with side entry and FOSV. Made up TDS. RIH with 30' Conductor to 201,7 m MD and adjusted setting depth according to marking on pipe releative to Centralizer deck." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Performed elevation check releative to F-15 using ROV and digiquartz, 18 mm deviation - ok. Recorded x/y inclinometer readings 0,0/0,2." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made up cement hose to pump in sub. Flushed lines. Performed line test agianst lo-torque valve to 200 bar / 5 min - ok." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated 28 m3 SW at 1500 lpm / SPP 0 bar." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped indicator pill (LCM). Not able to suck effectively from pit. Changed mudpump, but problems prevailing. Mudpump strainers plugged by LCM. Total LCM pill pumped 3,5 m3. Displaced LCM pill to string by pumping 3,6 m3 seawater." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Lined up to cement unit. Mixed and pumped 55 m3 1,54 sg xlite cement slurry at 920 lpm / CUP 21 bar. Observed cement return at seabead with ROV. Block weight declined from 101 MT to 97 MT during cementing." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Displaced cement with 6,2 m3 SW at 480 lpm / FCP 19 bar. Bled off pressure on cement unit - no backflow observed." "On 2009-04-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Waited on cement to set up. At 22:00, checked inclinometer x/y readings 0,2/0,12. Weight in block 97 MT. Issued notice for shut in of adjacent wells at 23:30." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Waited on cement to set up. Meanwhile performed toolbox talk for disconnecting landing string. Checked cement sample - ok." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Slacked off weight to neutral, i.e. 80 MT. Checked inclinometer x/y readings 0,02/0,13. Opened ball valve on CART. Bled off pressure above upper FOSV. Relased CART with 5 clockwise turns while observing conductor housing with ROV. Broke and laid down cementing stand. Picked up and made up 5 1/2' HWDP single, inserted sponge ball and made up single." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 188m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped sponge ball at 2000 lpm to clean string. Confirmed adjacent wells de-pressurized at 02:00." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with CART/stinger on 5 1/2' HWDP from 188 m to 50 m MD. Meanwhile installed CTS pump/funnel on conductor housing using aft crane and ROV." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pulled master bushing. Pulled CART through RT. Installed master bushing. Set down CART on master bushing. Removed inclinometer. Screwed out 5 1/2' HWDP single on top of CART. Rigged up C-plate in rotary, and hung off aluminium string on clamp. Broke and laid out CART." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with 5 ea aluminium singles using clamps, C-plate, tugger and chain tongs. Rigged down C-plate. Cleared drillfloor." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleared drillfloor. Put aluminium pipe in basket." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Held toolbox talk for making up BHA. Laid 26' bit/stab/motor on HTS." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk/handover meeting." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: Made up 26' drilling BHA comprising of 26' bit/stab/motor, GWD and powerpulse. Established scribeline from bent sub to MWD and recorded correction. Made up UBHO and adjusted landing sub as required. Made 8 1/4' DC stand and DC/jar stand. Recessed operation for TDS service/repair." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 136m. The activity was categorized as 'interruption -- other' and lasted for 8.2 hours. Operational details: Changed around stabilizing liners on TDS due to observed wear on drillpipe couplings. Observed rear liner crest more worn than front liner crest. Discussed options. Carried out rig repair of worn liner, i.e. clad welding. Installed modified liner crests on TDS. Comment : New stabilizer liners ordered from rig 30/1-09. Order sendt from Maersk office in town to supplier 8/4-09." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 175m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Moved diverter away from setback. RIH and stabbed 26' BHA into 30' conductor assissted by ROV. RIH to 175 m MD. ROV hooked up to CTS hose." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 175m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Made up TDS to test modified stabilizing liner on TDS. Observed scores on DP coupling when rotating pipe. Discussed situation. Opened IBOP and rotated pipe - observed no contact between dies and DP coupling. Decided to continue operation without repair/modifications." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 201m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Removed masterbushing and installed auto slips. Staged up pumps for washing down inside 30' conductor. Observed large shocks in drillstring. Ran ROV to observation position by CTS. RIH to 180 m MD, no hang ups observed. Staged up pumps to 3500 lpm and commenced rotation at 60 rpm. Washed down and tagged shoe/top of cement at 201 m MD." "On 2009-04-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 207m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Drilled cement and shoe. Parameters : Flow 2300-3500 lpm / SPP 48-95 bar / 40 RPM / WOB < 1 MT / Torque 2-3 kNm. Broke through shoe at ~203 m MD. Cleaned out rathole down to 207 m MD, reamed back every 2 m drilled." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 207m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Reciprocated across rathole and shoe 4 times. Swept hole with 20 m3 hivis pill." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 26' hole from 207 m to 217 m MD. Drilling parameters : Flow 3500 lpm / SPP 98 bar / 40 RPM / WOB < 1 MT / Torque 2-3 kNm. Secured string on Centralizer deck. Performed gMWD survey - out of specification. Continuos MWD survey 0-0,57 deg." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 228m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 26' hole from 217 m to 228 m MD. Drilling parameters : Flow 3500 lpm / SPP 48-95 bar / 40 RPM / WOB < 1 MT / Torque 2-3 kNm. Observed erratic string and torque peaks of 6-7 kNm at 227 m MD. Secured string on Centralizer deck. Performed gmWD survey - out of specification. MWD survey inclination 0,21 deg." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 231m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 26' hole from 228 m to 231 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 1-2 MT / Torque 2-3 kNm. Observed lose guide on automatic slips. Picked off bottom and stopped drilling." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 231m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed automatic slips from rotary for repair. Continued operation with manual slips." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 233m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 26' hole from 231 m to 233 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 1-2 MT / Torque 2-3 kNm. Secured string on Centralizer deck. Performed gMWD survey - out of specification. MWD survey inclination 0,26 deg." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 239m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 26' hole from 233 m to 239 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 3-5 MT / Torque 2-4 kNm." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 245m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 26' hole from 239 to 245 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 3-5 MT / Torque 2-4 kNm. Secured DP at Centralizer deck. Performed gMWD survey - accepted (inc 0,24 / azi 238 deg)." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 245m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Reamed interval 230-246 m MD in order to reduce inclination. Parameters : Flow 3500 lpm / SPP 97 bar / 40 RPM / Torque 2-4 kNm." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 244m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Rigged up WL for performing singel shot survey." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 244m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Ran singel shot survey. Landed gyro in UBHO at 208 m MD and performed survey. POOH with WL." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 244m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Rigged down WL equipment." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 246m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Reamed interval 222-246 m MD in order to reduce inclination. Parameters : Flow 3500 lpm / SPP 95 bar / 140 RPM / Torque 2-4 kNm. Pumped 2 x 10 m3 hivis pills. Reduced iclination from 0,53 deg to 0,16 deg." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 257m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 26' hole from 246 m to 257 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 3-5 MT / Torque 2-4 kNm. Secured DP at Centralizer deck. Performed gMWD survey - accepted. Pumped 10 m3 hivis pill." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 257m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Changed to slimmer type dies in TDS pipe handler in order to minimize scoring of DP couplings." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 298m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 26' hole from 257 m to 298 m MD. Flow 3100-3500 lpm / SPP ~100 bar / 40 RPM / WOB 2-3 MT / Torque 2-4 kNm. Secured DP at Centralizer deck and performed gMWD survey every singel drilled. Pumped hivs every singel." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 298m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Rigged up WL for performing singel shot survey. Marked pipe and rotary for tooface orientation." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 298m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Ran singel shot survey. Landed gyro in UBHO at 256 m MD and performed survey. Adjusted toolface to ~132 deg and repeated surveys as required. POOH with WL." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 298m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Rigged down WL equipment. Made up TDS and performed gMWD survey." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 298m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Inserted automatic slips (after repair job)." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 298m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Perfomed gMWD survey. Staged up pumps to 3000 lpm for sliding." "On 2009-04-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 328m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Initiated kick off according to DDs instructions. Drilled/slided from 298 m to 328 m MD. Drilling parameters : Flow 3000 lpm / SPP ~75 bar / 87-121 RPM / WOB 2-10 MT / Torque 1-4 kNm. Performed gMWD survey at 316 m MD." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 338m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Took 2 gMWD surveys at 328 m MD. Drilled 26' hole / slided from 328 m to 338 m MD. Drilling parameters : Flow 3000 lpm / SPP ~82 bar / 83 RPM / WOB 5-7 MT / Torque 3 kNm. Perfomed 3 gMWD surveys at 338 m MD. Obtained survey within specification on 3rd attempt." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 354m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 26' hole / slided from 338 m to 354 m MD. Drilling parameters : Flow 3000 lpm / SPP ~75 bar / ~85 RPM / WOB 5-6 MT / Torque 3-5 kNm. Secured DP at Centralizer deck and took gMWD survey at 354 m MD - ok." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 390m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled 26' hole / slided from 354 m to 390 m MD. Drilling parameters : Flow 3000 lpm / SPP 50-105 bar / 90-180 RPM / WOB 5-10 MT / Torque 4-8 kNm. Secured DP at Centralizer deck and took gMWD survey as instructed by DD." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 459m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 26' hole / slided from 390 m to 459 m MD. Drilling parameters : Flow 3500 lpm / SPP 50-112 bar / 90-180 RPM / WOB 5-10 MT / Torque 4-7 kNm / ROP 40 m/hr. Pumped 2-3 hivis pills per stand." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 459m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Rigged up WL equipment to run gyro." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 459m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Ran WL gyro. Landed gyro in UBHO at 420 m MD and performed survey. Experienced noise interference downhole. POOH with WL gyro and changed setting from North seeking to line of sight. RIH with gyro and landed in UBHO. Perfomed survey. POOH with WL gyro, performed contiunous survey on way out." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 459m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Rigged down WL equipment." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 620m. The activity was categorized as 'drilling -- drill' and lasted for 10.0 hours. Operational details: Drilled 26' hole / slided from 459 m to 620 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 85-177 bar/ 130-220 rpm / WOB 4-15 MT / Torque 5-12 kNm / ROP 30-60 m/hr. Performed gMWD/MWD survey on every single. Pumped 2-3 hivis pills per stand." "On 2009-04-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 660m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 26' hole / slided from 620 m to 660 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 95-180 bar/ 130-220 RPM / WOB 4-15 MT / Torque 5-12 kNm / ROP 30-50 m/hr. Performed gMWD/MWD on every connection. Pumped 2-3 hivis pills per stand." "On 2009-04-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 742m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 26' hole / slided from 660 m to 742 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 90-200 bar/ 130-220 RPM / WOB 15-20 MT / Torque 12-15 kNm / ROP 20-40 m/hr. Performed gMWD/MWD on every connection. Obtained 3rd consecutive quality survey MWD versus gMWD. Pumped 2-3 hivis pills per stand." "On 2009-04-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 26' hole / slided from 742 m to 798 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 105-200 bar/ 130-220 RPM / WOB 15-20 MT / Torque 12-15 kNm / ROP 15-25 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand." "On 2009-04-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 862m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled 26' hole / slided from 798 m to 862 m MD. Drilling parameters : Flow 3100-4500 lpm / SPP 105-200 bar/ 130-220 RPM / WOB 15-20 MT / Torque 12-15 kNm / ROP 15-35 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand." "On 2009-04-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 862m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Reamed/reciprocated last stand 3 times in order to clean hole before entering Utsira. Pumped 15 m3 hivs pill. Parameters : Flow 4000-4500 lpm / SPP 137-174 bar/ 140-170 RPM / Torque 3-5 kNm." "On 2009-04-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 893m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 26' hole / slided from 862 m to 893 m MD. Drilling parameters : Flow 4500 lpm / SPP ~190 bar/ 130 RPM / WOB 10-20 MT / Torque 3-5 kNm / ROP 10-20 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand. Encountered top of Utsira at 892 m MD observed by drilling break." "On 2009-04-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1090m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled 26' hole / slided from 893 m to 1090 m MD. Drilling parameters : Flow 3500 lpm / SPP 110-130 bar/ 100 RPM / WOB 5-10 MT / Torque 0-4 kNm / ROP 50-130 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand." "On 2009-04-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1148m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled 26' hole / slided from 1090 to 1148 m MD. Drilling parameters : Flow 4000-4500 lpm / SPP 150-190 bar/ 130-220 RPM / WOB 10-20 MT / Torque 0-20 kNm / ROP 10-20 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand. Encountered hard stringers at 1116, 1124 and 1134 m MD" "On 2009-04-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1265m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 26' hole / slided from 1148 m to 1265 m MD. Drilling parameters : Flow 3000-4000 lpm / SPP 150-180 bar/ 115-200 RPM / WOB 8-20 MT / Torque 5-15 kNm / ROP 10-20 m/hr. Reamed 2 last stands drilled in order to cater for drilling the Skade formation. Pumped 2-3 hivis pills per stand." "On 2009-04-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- drill' and lasted for 6.2 hours. Operational details: Drilled 26' hole / slided from 1265 m to section TD at1400 m MD. Drilling parameters : Flow 3500-4500 lpm / SPP 130-190 bar/ 100-170 RPM / WOB 5-20 MT / Torque 5-20 kNm / ROP 40-150 m/hr. Pumped 2-3 x 30 m3 hivis pills per stand. Perfomed MWD survey on every connection. Maintained toolface highside when drilling Skade sand. Top Skade at 1234 m MD and base Skade at 1364 m MD." "On 2009-04-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated hole clean. Pumped 2 x 30 m3 hivis pills. Reciprocated stand between 1400 m and 1384 m MD. Parameters : Flow 4500 lpm / SPP 180-190 bar / 170-220 RPM / Torque 9-14 k Nm." "On 2009-04-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Displaced well partly to put 1,40 sg KCl mud to above Utsira formation. Pumped a total of 252 m3 KCl mud. Parameters : Flow 4500 lpm / SPP 205-215 bar / 170 RPM / Torque 7-14 kNm." "On 2009-04-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1223m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: POOH with 26' drilling BHA from 1400 m to 1223 m MD. Took 30-50 MT overpull when pulling through Skade sand. Worked string with rotation/flow as limited by torque and overpull. Paramaters : Flow 200-1000 lpm / SPP 2-5 bar / 20-30 RPM / Torque 10-35 kNm. String free with normal weight when bit above Skade sand." "On 2009-04-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 958m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 26' drlling BHA from 1223 to 958 m MD." "On 2009-04-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 916m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Encounterd thight hole at 958 m MD, took 20-30 MT overpull. Worked string with rotation/flow as limited by torque and overpull. Parameters : Flow 200-800 lpm / SPP 2-5 bar / 30 RPM / Torque 6-28 kNm." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 887m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Continued working string from 916 m to 887 m MD. Worked string with rotation/flow as limited by torque and overpull. Parameters : Flow 200 lpm / SPP 2-3 bar / 30 RPM / Torque 6-33 kNm." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 540m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 26' drilling BHA from 887 m to 540 m MD. Worked thight area from 650 m to 640 m MD." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 495m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Displaced well above 500 m MD to 1,40 sg KCl mud while pullling stand. Pumped a total of 143 m3 mud. Parameters : Flow 4500 lpm / SPP 200-210 bar / 30 RPM (string) / Torque 4-7 kNm. Issued notice to shut-in adjacent wells at 03:30." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 250m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 26' drilling BHA from 495 m to 250 m MD. Worked tight area from 450 m to 430 m MD." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 250m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: At 250 m MD, topped up well by pumping 15 m3 1,40 sg KCl mud. Flow 1800 lpm / SPP 34 bar. Meanwhile performed toolbox talk for pulling BHA." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 146m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 26' drilling BHA from 250 m to 146 m MD. Removed PS-21 slips and installed master bushing. Confirmed adjacent wells shut in at 05:45." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: POOH with 26' drilling BHA from 146 m MD to 136 MD. Observed with ROV when comming through CTS funnel / 30' conductor." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH and racked back stand of 8,25' DC. Broke and laid out jar." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Broke and racked back stand of 8,25' DC and stand of 9,25' NMDC. Broke connection between gMWD and MWD, retrieved gyro insert, re-made connection. Attempted to rack to rack back 26' drilling BHA in derrick - negative - too high weight in PRS. Large amounts of clay trapped on BHA." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for breaking BHA." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Broke and laid out UBHO, MWD, GMWD and stab/motor/26' bit. Meanwhile removed CTS funnel from conductor using aft crane assisted by ROV." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Cleared and tidied drillfloor. Prepared for rigging casing running equipment." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Removed DP elevator and drilling bails. Moved casing casing tong and frame to IR tracks. Hooked up hydraulics to casing tong." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to derrick inspection. Isolated equipment." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed inspection of derrick and TDS using manrider." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Made up LaFleur circulating tool. Installed long bails. Installed 310 MT BX elevator and hooked up hydraulics. Meanwhile ROV performed digiquartz measurement of conductor elevation releative to F-15 - 1 mm deviation." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk for running 20' casing. Made adjustments on Lafleur spacing." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Picked up 20' shoe joint. Hung off in rotary and secured with dog collar. Tested float for flowthough - ok. Picked up and made up 20' intermediate joint. Adjusted stabbing arm and casing tong. Applied threadlock and made up connection to 46000 ft lbs (max available torque). RIH." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up 20' landing collar joint. Checked threads. Applied threadlock and made up connection to 46000 ft lbs. Found spacing to make up mark to be approx 5 mm short. Discussed situation and decided to continue operation." "On 2009-04-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 78m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing w/centralizers from 40 m to 78 m MD. Checked floats for inflow - ok." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing w/centralizers from 78 m to 139 m MD." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Stabbed 20' casing into conductor. Used ROV push buckle to assist. Issued instruction to start production in adjacent wells at 02:28." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing from 150 m to 214 m MD. Filled casing with KCl mud every 5th joint." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed master bushing. Installed PS-30 slips which was challenging due to large OD casing through RT." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 292m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing from 214 m to 292 m MD. Filled casing with KCl mud every 5th joint." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 314m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing from 292 m to 314 m MD. Filled casing with 1,40 sg KCl mud every 5th joint." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 314m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held handover meeting." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 448m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing from 314 m to 448 m MD. Filled casing with 1,40 sg KCl mud every 5th joint." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Took 20 MT weight at 448 m MD. Attempted to pass restriction 4 times - negative. Broke circulation and worked string down to 460 m MD pumping 1,4 sg mud at 660 lpm / SPP 17 bar. Circulated bottoms up pumping seawater at 1550 lpm / SPP 24 bar. Observed cuttings returns to seabed." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 497m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing from 460 m to 497 m MD. Observed loose link-tilt clamp on bails." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 497m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Prepared permit for manriding. Isolated drillfloor equipment. Re-tightned link tilt clamp. De-isolated equipment." "On 2009-04-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1066m. The activity was categorized as 'drilling -- casing' and lasted for 9.2 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing from 314 m to 448 m MD. Filled casing with 1,40 sg KCl mud every 5th joint. Tight spot at 640 m to 652 m MD, ~15 MT drag but no circulation needed." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: RIH with 20' 133# N80 Tenaris ER casing from 1066 m to 1238 m MD. Filled casing with 1,40 sg KCl mud every 5th joint. Counted joints left on deck - 18 - ok." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Broke out Lafleur packer. Rigged down 310 MT BX elevator. Rigged down long bails. Installed drilling bails and DP elevator. Removed equipment from drillfloor." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up 18 3/4' wellhead. Removed protective cap. Washed and checked threads. Made up 18 3/4' WH to 20' casing." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed PS-30 slips from rotary and installed outer ring." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Attempted to RIH with 20' casing / 18 3/4' WH - negative. Worked to free pipe with alternating up/down weights, 50 MT set down / 60 MT overpull - negative - 20' casing differential stuck. String movement < 50 cm. Set down 50 MT weight. Installed split bowl and set casing in slips. Discussed situation, decided to attempt making up TDS and displace well from 1,40 sg KCl mud to seawater." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Screwed in TDS to pup joint on CART while observing movement on CART. Managaed to get torque wrench in position without jeapordizing CART make up. Made up TDS." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: Staged up pumps to 660 lpm, verified returns to seabed. Staged up pumps to 2000 lpm / SPP ~30 bar." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Attempted to free string while circulating at 2000 lpm. Set down / overpull 60/60 MT. Increased set down weight to 80 MT and observed string comming free. Took up/down weights 270/220 MT. Cummulative volume of seawater pumped ~300 m3." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1238m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Reduced flowrate to 500 lpm and reciprocated string while rigging down and removing casing tong. RIH to 1249 m MD and hung off wellhead in manual slips." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1249m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Filled gap between wiper plugs through port on CART. Verified free rotation of CART tool." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1249m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Made up TDS to stand of 5 1/2' HWDP and CART. Worked the string while investigating activity on seabed." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed split bushing from RT. Ran 18 3/4' WH CART past rotary. Installed master bushings." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1383m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 20' casing / 18 3/4' wellhead on 5 1/2' HWDP from 1251 m to 1383 m MD. Washed down with 1000 lpm / SPP 14 bar." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Worked through tight area from 1383 m to 1389 m MD ~25 MT drag. Washed down with 2000 lpm / SPP 24 bar." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up cement head and continued working tight spot down to 1289 m MD. Landed and locked 18 3/4' wellhead in 30' conductor housing at 139,72 m MD by setting down string weight (WH Datum @ 138.94 m RT). Performed 50 MT overpull test on wellhead - ok." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held prejob meeting for cementing 20' casing. Hooked up cement hose to cement head." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Verified line up. Tested cement line to 200 bar - ok." "On 2009-04-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Dropped 1 3/4' ball for bottom wiper plug. Sheared bottom wiper plug with 50 bar. Mixed and pumped 90 m3 1,56 sg SSA cement (lead 1) cement at 1100 lpm / CUP 23 bar. Mixed and pumped 120 m3 1,56 sg cement (lead 2) at 1100 lpm / CUP 21 bar." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Mixed and pump 113 m3 1,56 sg cement (lead 2) at 1100 lpm / CUP 21 bar. Mixed and pumped 25 m3 1,92 sg tail slurry at 800 lpm / CUP 20 bar." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced cement to drillfloor with 890 liters. Dropped dart. Displaced 3000 liter pumping with cement unit. Observed shear of lower wiper plug with 180 bar." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Lined up to pump with mud pumps. Stepped up pumps to 3000 lpm. Pressure rose from 4 bar to 89 bar during displacement. Displaced cement with 9661 strokes (177 strokes less than theoretical). Bumped plug with 170 bar, i.e. 80 bar more than FCP at 3000 lpm. No firm confirmation of cement returns to seabed during displacement, but steady fluid return was observed during the operation." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up to cement unit. Bled back to cement unit, in total 2,3 m3 before backflow stopped. Issued instruction to shut in adjacent wells at 04:40." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: While depressurising wells. Rigged down cement hose and flushed same. Brought 2 x tension cylinders from moonpool to Centralizer deck. Brought ROV to surface for collecting WH cap." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Mounted tension cylinders on Centralizer deck. ROV brought WH cap to seabed. Verified adjacent wells shut in at 06:30." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released CART with 5 clockwise turns." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for laying out cement head." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke and laid down cement head. Hooked down hydraulics. laid out cement head on HTS." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Inserted sponge balls in string. Pumped sponge balls at 500 lpm / SPP 1 bar. POOH with CART on 5 1/2' HWDP from 137 m MD to surface. Broke and laid out CART." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk for installing tension cylinders." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Brought 2 x tension cylinders from Weatherdeck to Centralizer deck. Mounted tension cylinders on Centralizer deck. Meanwhile prepared for running HPDR. Notice given to start production at 09:15. Started production in adjacent wells at 13:30." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Rigged up for running HPDR. Brought riser spider to drillfloor and hooked up same. Brought tensioning equipment to drillfloor. Meanwhile cleaned pits for reception of OBM." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk for picking up HPDR." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Brought TBC / double 'A' from Cantilever to drillfloor by simultaneous lift by deck crane and TDS. Retracted TDS and set down TBC on drillfoor." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Function tested and performed pre-operational checks on TBC according to Vetco procedure. Brought boat collission stool from drillfloor to Centralizer deck. Installed RLGF on wellhead using aft crane and ROV. Verified production shut in of adjacent wells at 18:50." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran TBC / double 'A' through moonpool, Weatherdeck and XMT deck and hung off in spider." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Brought double 'B' from Cantilever to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange type C from TBC /double 'A'. Landed double 'B' onto double 'A'." "On 2009-04-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Made up riser flange using bolt tensioner tool." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Tested flange to 3000 psi with handpump. Installed bolt caps and fairings on flange." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 34m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: RIH with HPDR and located TBC on Centralizer deck. Ran guidewires. Caught guidewires through well slot and threaded same through ROV hooks above HPDR riser. Ran 6T tugger/guidewire to seabed and attached same. Ran 10T tugger/guidewire to sealevel." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran HPDR riser to 52 m MD and hung off in spider." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Brought double 'C' from Cantilever to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange on double 'B'. Inspected and refurbished flanges." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Landed double 'C' onto double 'B'. Made up riser flange using bolt tensioner tool. Tested flange to 3000 psi with handpump." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed bolt caps and fairings. Ran HPDR to 82 m MD and hung off in spider." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Brought double 'D' to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange type 'C' from double 'C'. Cleaned and refurbished flanges. Landed double 'D' onto double 'C'." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Made up riser flange using bolt tensioner tools." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed bolt caps and fairings." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Ran HPDR from 82 m to 105 m MD." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Brought BOP/tension joint double 'E' to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange type 'C' from double 'D'. Cleaned and refurbished flanges. Landed double 'E' onto double 'D'." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Made up riser flange using bolt tensioner tools. Installed bolt caps and fairings." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Rigged tuggers for removing riser spider. Split and removed riser spider." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ran HPDR from 105 m to 130 m MD. Installed outer ring and master bushing in rotary." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up stand of 5 1/2' HWDP to TDS and Claxton tool." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Run in with HPDR and stabbed TBC into RLGF. Observed VX ring out of position. Used ROV arm to push VX ring in correct position. Verified correct orientation of valve panel on TBC. Observed sufficient connector swallow over wellhead in RLGF window." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Re arranged RLGF slings. Split RLGF and removed by ROV. Meanwhile prepared to install hatches and built scaffolding." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Landed TBC on 18 3/4' wellhead, set dwon 15 mT on wellhead. Ran hotstab and engaged same in TBC receptacle. Locked TBC by applying 3000 psi. Issued intruction to start up adjacent wells at 17:00." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Took 15 MT overpull, i.e. 140 MT on block to test tie-back connector - ok. Installed hathces on Weatherdeck. built scaffolding on Weatherdeck to access Claxton tool." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held toolbox talk for pressure test. Lined up cement unit to pump down string. Topped up HPDR with 8 m3 seawater. Instatalled weco cap on Calxton tool." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pressure tested HPDR and 20' casing to 20/195 bar 5/10 min - ok. volume pumped and bled back 2850 liter. Maintained 140 MT block weight when pressuring up and bleeding off. Observed sudden jump in block weight (10 MT) when pressuring up. Investigated and found that plug of cement had been released through the 30' conductor cementing ports (observed by ROV)." "On 2009-04-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Installed centralizers, plastic and brass bushings in Centralizer deck. Meanwhile released BOP NT-2 connector from stump." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed boat collision stool at Centralizer deck. Installed and alligned contact ring. Meanwhile released BOP NT-2 connector from stump." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Hooked up hydraulics to tension cylinders on Centralizer deck." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Installed tensioning assembly half hubs. Oriented half hubs. Made up half hubs to tension ring. Ran tension cylinders and coupled 2 ea to tensioning assembly." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Coupled 2 ea tension cylinders to tensioning assembly. Transfered tension from block to tensioning cylinders. Applied 90 bar on tension cylinders, i.e. 150 MT tension." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk for releasing Claxton tool." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Broke studs on Claxton tool using J-gun. Pulled out Claxton tool and laid out same." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Modified scaffolding on Weatherdeck for skidding BOP. Meanwhile retrieved RLGF from seabed using port crane assisted by ROV. Retrieved 10MT guidewire/tugger." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Moved BOP to wellcenter, landed BOP on HPDR and started nipling up NT-2 connector. Made up swadge to TDS and tested upper/lower IBOP and kelly hose - ok." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Installed bell nipple and diverter." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Got problems with HPU due to overheating of hydraulic oil. Reverted to planned maintenance activity on TDS. Changed springs on centralizer bearing and die carrier. Meanwhile allowed hydraulic oil on HPU to cool." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Made up pulling tool for nominal seat protector. RIH with NSP pulling tool from surface to 140 m MD. Latched onto NPS and pulled free with 10 MT overpull. Filled BOP with seawater. POOH with NSP from 140 m MD to surface. Set back RT with NSP." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up and made up 18 3/4' BOP test plug. RIH with test plug and landed same in wellhead at 140 m MD." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Lined up cement unit and flushed line to trip tank. Lined up to BOP. Closed UPR. Tested BOP connector to 20/345 bar 5/10 min - ok. Volume pumped and bled back 450 liters." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: As part of planned maintenance ; changed 1 die block on TDS to slimmer type." "On 2009-04-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up RT/NSP and made up to stand of 5 1/2' DP." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with NSP to 140 m MD and set according to Vetco instructions." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with NSP RT from 140 m MD to surface. Broke and laid down RT." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for making up 17 1/2' drilling BHA." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Made up 17 1/2' drilling BHA comprising of 17 1/2' bit/PDX5/stab, Powerpulse, ARC, 17' NM stab and stand of 9 1/2' NMDC. Made up x-over to DC." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Picked up stand of 8,25' DC. Broke and laid out 8,25' DC singles for onshore inspection." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Broke and laid out 8,25' DC singles. Ran stand of 8,25' DC, broke and laid out 2 singels." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Picked up and made up 2 x 8,25' DC and jar. Picked up and made up 2x8,25' DC and intensifier." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 115m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Found sheared bolt on actuator for PS-21. Removed PS-21 for repairs. Installed master bushing. Repaired PS-21 slips." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 194m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP from 115 m to 194 m MD. Used manual slips. Meanwhile repaired PS-21 slips." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 194m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Isolated TDS for maintenance. Changed out TDS centralizer bushings. Changed die carriers on TDS torque wrench." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 194m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed masterbushing and installed PS-21 slips." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP from 194 m to 1000 m MD." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Filled drillstring with SW. Tested MWD - ok." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1323m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP from 1000 m to 1323 m MD." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1323m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Performed choke drill." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1323m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held toolbox talk for drilling ahead and dispalcing to 1,40 SG OBM." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Washed down from 1323 m and tagged top of cement/plugs at 1359 m MD. Parameters : Flow 3200 lpm / SPP 64 bar / 30 RPM / Torque 10-13 kNm." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held toolbox talk / handover meeting." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Lined up for displacement and drained U-tube in surface equipement. Posted personnel." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: While drilling on wiper plugs at 1359 m MD - displaced well from SW to 1,40 sg OBM. Displaced mainfold and C/K lines to OBM. Drilling parameters : Flow 3200 lpm / SPP 60 bar increasing to 125 bar / 60 RPM / Torque 12 kNm decreasing to 8 kNm / WOB ~5 MT / ECD 1,38." "On 2009-04-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Drilled on cement plugs at 1359 m MD. Little or no progress was made. Drilling parameters : Flow 3200 lpm / SPP 123 to 118 bar / 40-60 RPM / WOB 5-10 MT / Torque 9-12 kNm. When increasing WOB to 10 MT - observed high stick/slip on MWD." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Drilled on cement plugs at 1359 m MD. Increased WOB to 15 MT. Drilling parameters : Flow 3200 lpm / SPP 115 bar / 40-70 RPM / WOB 6-15 MT / Torque 9-20 kNm. Meanwhile added barite to active to raise mudweight." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Bit stalled out at 35 kNm at 1360,6 m MD. Released torque in string. Worked string free with 20 MT overpull - string free with no excessive drag. Reamed tight area." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1389m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Drilled shoetrack from 1360 m to 1389,5 m MD. Drilling parameters : Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB ~5 MT / Torque 12-15 kNm / ECD 1,39 sg / ROP 12 m/hrs. Broke through shoe at 1389,7 m MD. Meanwhile rigged up Weatherford casing tong on drillfloor fore." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1395m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned out rathole down to 1393 m MD in increments of 2 m pulling back into shoe. Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB < 1 MT / Torque 6-10 kNm / ECD 1,39 sg." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Cleaned out 26' rathole from 1393 m to 1400 m MD. Parameters : Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB < 1 MT / Torque 6-10 kNm / ECD 1,39 sg." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1403m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 17 1/2' hole from 1400 m to 1403 m MD prior to FIT. Drilling paramaters : Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB 3 MT / Torque 11 kNm / ECD 1,39 sg." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1403m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 3.0 hours. Operational details: Ciruclated 3 x bottoms up to get even mudweight 1,39 in/out prior to FIT. Reciprocated stand. Flow 4000 lpm / SPP 170 bar / 30 RPM." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1403m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped and spotted LCM pill across open hole at 2200 lpm / SPP 46 bar." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1363m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.2 hours. Operational details: POOH from 1403 m to 1363 m MD. Racked back stand. Made up kelly cock/side entry sub and flushed line. Tested line to 50 bar / 5 min - ok. Closed UPR." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1363m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Lined up to cement unit. Performed FIT to 1,60 EMW. Pumped 420 liter / CUP 29,6 bar. Bled back 460 liter." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1363m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Broke out and laid down kelly cock/side entry sub. Lined up to standpipe. Took SCRs. Filled sandtraps." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1403m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH to TD at 1403 m MD. Downlinked powerdrive prior to drilling ahead." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1405m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 17 1/2' section from 1403 m to 1405 m MD. Drilling parameters : Flow 4000 lpm / SPP ~180 bar / 60 RPM / WOB 5 MT / Torque 8-10 kNm / ECD 1,39 sg." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1405m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Cleared augers in shaker room due to stop/blockage. Auger stop caused by rubber." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1443m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 17 1/2' hole from 1405 m to 1443 m MD. Drilling parameters : Flow 4000-4300 lpm / SPP 180-197 bar / 60-150 RPM / WOB 4-10 MT / Torque 6-16 kNm / ECD 1,39-1,40 sg. Set powerdrive to 342 deg / 100%. Observed no reposonse from powerdrive - hold and slight drop, no steering." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1443m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Discussed situation. Produced alternative well projections for drilling ahead one more stand. Set powerdrive to 270 deg / 100%. Meanwhile pulled off bottom and reciprocated stand. Paramaters : Flow 2500-3000 lpm / SPP 73-105 bar / 30 RPM / Torque 7 kNm / ECD 1,40-1,45 as determined by weighing up mud." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1463m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 17 1/2' hole from 1443 m to 1463 m MD. Drilling parameters : Flow 4100 lpm / SPP ~195 bar / 120 RPM / WOB 2-7 MT / Torque 6-8 kNm / ECD 1,45-1,46 sg. Observed no left reposonse from powerdrive - hold and slight drop, no steering. Recessed drilling. Decided to POOH to change to back-up powerdrive." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1453m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Circulated hole clean and obtained even mudweight in/out. Parameters : Flow 4500 lpm / SPP~245 bar / Torque 6 kNm / ECD 1,47." "On 2009-04-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1453m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Flowchecked - well static. Pumped slug for POOH." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1435m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' BHA from 1453 m to 1435 m MD. Observed overpull of 10-15 MT at 1452 m MD. Worked string with 30 RPM as dictated overpull (10-15 MT) and torque (max 20 kNm). String free to move down. Normal drag obatained at 1435 m MD." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 174m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 1435 m to 174 m MD." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 174m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked - well static. Filled triptanks." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 116m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP/HWDP from 174 m to 116 m MD. Removed PS-21 slips. Installed master bushing." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 116m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Pulled and racked back stand of 8,25' DC/intensifier and stand of 8,25' DC/jar." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 17 1/2' BHA, racked on set back. Inspected bit and damaged Power Drive." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Drill crew hand over." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Toolbox talk prior to handling BHA, rig tongs required." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleared and cleaned rigfloor after POOH." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Broke off 17 1/2' bit from damaged Power Drive. Bit to be re-run. L/D Power Drive on deck." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: P/U new Power Drive, made up bit." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH from surface to 84m." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Stopped due to uncertainty of float status. Toolbox talk prior to POOH to check float." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH from 84m to 4m. Broke BHA, inspected float, twisted. Removed twisted float." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: RIH from 4m fo 27m, installed float sub and standard float on top of 17' NM string stabilizer. Rig tongs required." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH with 17 1/2' BHA from 27m to 115m." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Installed PS-21 slips dressed for 5 1/2' DP." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 559m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: RIH from 115m to 559m." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 559m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Tool box talk with on comming shift prior to RIH with 17 1/2' BHA on 5 1/2' DP from 559m." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1364m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: RIH from 559m to 1364m, emptying trip tank every 10 stand, filled pipe at 1000m." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1406m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Made up top drive and slided through 20' casing shoe to 1406m. No restrictions observed." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1463m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Took up/down weight, 135/121 ton, free rotation weight, 50 rpm, 127 ton. Started pumps and rotation, 3200 l/min, 137 bar, 50 rpm, 8-10 kNm. Washed from 1406m to tagging depth 1463m." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1463m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pulled 2m, established drilling parameters, 4300 l/min, 225 bar, 150 rpm, 8-10 kNm. Tagged with 2-4 ton, 4300 l/min, 228 bar, 150 rpm, 10-12 kNm." "On 2009-04-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1495m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled from 1463m to 1495m, 4490 l/min, 240 bar, 160 rpm, 9-12 kNm, WOB 2-5 ton, ROP 18-20 m/hr." "On 2009-04-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1515m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled from 1495m to 1515m, 4490 l/min, 240 bar, 160 rpm, 9-12 kNm, WOB 2-5 ton, ROP 15-20 m/hr." "On 2009-04-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1516m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled with reduced ROP, 10 m/hr, due to problems with injection of cuttings." "On 2009-04-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1516m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Pulled off bottom and circulated, due to problems with cuttings injection. 3500 l/min, 153 bar, 60 rpm, 7-9 kNm. Reciprocated pipe." "On 2009-04-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1567m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Back on bottom for drilling 17 1/2' hole from 1516m to 1567m. 4490 l/min, 240 bar, 160 rpm, 9-12 kNm, WOB 2-3 ton, ROP 19-20 m/hr. Meanwhile delivered cuttings to skip and trouble shot cuttings injecting system. Observed rubber in cutting pumps." "On 2009-04-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1640m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled 17 1/2' hole from 1567m to 1640m. 4490 l/min, 240 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 10-17 m/hr. Simultaneously P/U and build 2 stands of 13 3/8' casing set back. Malfunction occurred on alignment in FWD PRS. Emergency switch accidently activated during trouble shooting alignment problems on FWD PRS. Stop in operation while re-set (10 min)." "On 2009-04-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1734m. The activity was categorized as 'drilling -- drill' and lasted for 7.2 hours. Operational details: Drilled and steared 17 1/2' hole from 1640m to 1734m. 4490 l/min, 240 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr." "On 2009-04-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1809m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 17 1/2' hole from 1734m to 1809m. 4490 l/min, 245 bar, 160 rpm, 12-15 kNm, WOB 3-5 ton, ROP 15-17 m/hr." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1866m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled and steared 17 1/2' hole from 1809m to 1866m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1866m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Picked off bottom, circulated and reciprocated pipe while trouble shooting problems in cutting injection system. 3100 l/min, 140 bar, 60 rpm, 7-9 kNm." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1884m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and steared 17 1/2' hole from 1866m to 1884m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr. Cuttings to skip, while cleaning slurry pump." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1889m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled and steared 17 1/2' hole from 1884m to 1889m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 3-4 ton, ROP 15-17 m/hr. Cuttings pump back, injection re-established. P/U and build 5 stands of 13 3/8' casing and racked on set back during last 12 hrs." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1970m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' hole from 1889m to 1970m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr. Meanwhile MU 13 3/8' csg in stands. 09:00 broke two bolts on flushjoint elevator tilt cylinder. Secured and repaired flush joint elevator." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2062m. The activity was categorized as 'drilling -- drill' and lasted for 7.2 hours. Operational details: Drilled 17 1/2' hole from 1970m to 2062m. 4490 l/min, 253 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr. Plugging i CRI and conveyers. Meanwhile repaired flushjoint elevator on fwd PRS." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2062m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Pulled off bottom due to plugging on CRI and cuttings conveyers. Circulated and reciprocated pipe, 3000 l/min, 125 bar, 60 rpm, 9 kNm while sorting out CRI and conveyers." "On 2009-04-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2104m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 17 1/2' hole from 2062m to 2104m. 4490 l/min, 256 bar, 160 rpm, 11-13 kNm. WOB 2-4 ton, ROP 15-17 m/hr." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2155m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 17 1/2' hole from 2104m to 2155m. 4490 l/min, 258 bar, 160 rpm, 11-13 kNm. WOB 2-4 ton, ROP 15-17 m/hr." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2155m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pulled off bottom due to clearing CRI tank. Circulated and reciprocated pipe, 3000 l/min, 125 bar, 60 rpm, 9 kNm." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2179m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 17 1/2' hole from 2155m to 2179m. 4490 l/min, 258 bar, 160 rpm, 11-13 kNm. WOB 3-5 ton, ROP 15-17 m/hr. MU 3 stands of 13 3/8' casing last 12 hrs." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2267m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and steered 17 1/2' hole from 2179m to 2267m. 4490 l/min, 256 bar, 160 rpm, 11-13 kNm. WOB 2-4 ton, ROP 15-17 m/hr." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2361m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled and steered 17 1/2' hole from 2267m to 2361m. 4490 l/min, 258 bar, 160 rpm, 13-15 kNm. WOB 2-4 ton, ROP 15-17 m/hr." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2385m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and steered 17 1/2' hole from 2361m to 2385m. 4530 l/min, 277 bar, 180 rpm, 13-15 kNm. WOB 2-4 ton, ROP 15-17 m/hr. Problem with mud pump." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2385m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Picked off bottom due to wash out in mud pump 1 piston. Lost suction on mud pumps. Lined up for drilling with 2 mud pumps. Lost suction on CRI pump." "On 2009-04-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2414m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Problem cleared. Drilled and steered 17 1/2' hole from 2385m to 2414m. 4530 l/min, 277 bar, 180 rpm, 13-15 kNm. WOB 4-6 ton, ROP 15-17 m/hr." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2432m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled and steered 17 1/2' hole from 2414m to 2432m. 4500 l/min, 275 bar, 180 rpm, 13-23 kNm. WOB 6-8 ton, ROP 15-17 m/hr. MWD tool battery empty. All signals work when pumps on, no signal without pumping." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2432m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Picked off bottom and reamed 1 joint due to stick slip and shocks at level 2 in BHA." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2467m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and steered 17 1/2' hole from 2432m to 2467m. 4500 l/min, 275 bar, 160 rpm, 20-26 kNm. WOB 6-8 ton, ROP 10-15 m/hr. Simultaneously mU and racked 15 stands of 13 3/8' casing in derrick over last 24 hrs, 27 stands in total." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and steered 17 1/2' hole from 2467m to 2550m. 4500 l/min, 275 bar, 150 rpm, 17-19 kNm. WOB 4-7 ton, ROP 15-17 m/hr." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2574m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled and steered 17 1/2' hole from 2550m to 2574m. 4500 l/min, 275 bar, 150 rpm, 17-19 kNm. WOB 4-7 ton, ROP 15-17 m/hr." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2574m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Picked off bottom, serviced TDS, 2500 l/min, no rotation." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and steered 17 1/2' hole from 2574m to 2616m, TD of section. 4500 l/min, 275 bar, 150 rpm, 17-19 kNm. WOB 4-7 ton, ROP 15-17 m/hr." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Circulated 2000 ltrs at bottom. 4500 l/min, 275 bar, 160 rpm, 17-19 kNm. 2,5m3/hr mud loss." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: Circulated hole clean. 4490 l/min, 280 bar, 150 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m. Had 1,5m3/hr mud loss during circulation." "On 2009-04-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated hole clean. 4490 l/min, 280 bar, 150 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m. Had 1m3/hr mud loss during circulation, increasing to 1,5m3/hr. Started to mix LCM pill." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Circulated hole while waiting on LCM pill mixing. 3500 l/min, 180 bar, 50 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated hole while waiting on hi-vis pill mixing. 3500 l/min, 180 bar, 50 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2535m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: -" "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2351m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Pumped LCM pill as we pullled 17 1/2' BHA from 2495m to 2351m. 900 l/min, 20 bar, no rotation." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2328m. The activity was categorized as 'drilling -- ream' and lasted for 8.0 hours. Operational details: Pulled from 2351m to 2328m. Observed 30 ton overpull. Observed pack off repetedly. Worked string from 2360m to 2328m, 0-4500 l/min, 0-270 bar, 0-120 rpm, 0-25 kNm, 0-30 ton over pull." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2360m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated bottom up, 4500 l/min, 270 bar, 120 rpm, 10-13 kNm. Reciptocated pipe between 2360m and 2346m." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2360m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled from 2360m to 2346m. No pumping no rotation. Pulled 2m lowered 1m in steps. Took weight at 2350m." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2293m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Lowered string to 2356m, started to backream from 2356m to 2293m. Increased pumps tn steps to 2000 l/min, 65-70 bar, 80 rpm, 11-13 kNm. Layed out 1 joint of 5 1/2' DP." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2250m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: Back reamed from 2293m to 2250m with increased flow to 3600 l/min, 188-190 bar, 80 rpm, 12-15 kNm." "On 2009-04-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2250m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Increased parameters to 4500 l/min, 275 bar, 180 rpm, 13-15 kNm." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2250m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated 2 x bottom up, 4500 l/min, 275 bar, 180 rpm, 13-15 kNm. Observed increase in cuttings at shakers when 1 x bottom up. Reciprocated pipe between 2250m and 2213m." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2213m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flow checked well, 300 l/hr static loss." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2090m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH from 2213m. Pulled 4 stands increasing over pull to 25-30 ton. Observed Trip tank 200 l above expected level. Checked level in drill string: 20m below RKB." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2252m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: RIH to 2248m, took 10-12 ton, started pumps in steps to 3600 l/hr, RIH to 2252m." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2252m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flow checked prior to back reaming. 360 l/min static loss." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2252m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Established parameters for back reaming, 4500 l/min, 275 bar, 180 rpm, 12-14 kNm." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2212m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Back reamed from 2252m to 2212m. 4500 l/min, 275 bar, 180 rpm, 12-14 kNm." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2090m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Back reamed with 17 1/2' BHA from 2212m to 2090m. 4500 l/min, 265 bar, 180 rpm, 12-14 kNm." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2090m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Set Power Drive to neutral." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2013m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: Back reamed from 2090m to 2013m. 4500 l/min, 260 bar, 180 rpm, 12-14 kNm." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2013m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Packed off stright afher connection. Took 10-15 ton over pull at 2013m. RIH to 2021m. Established circulation, staged pumps to 4500 l/min, 265 bar, 150 rpm, 10-15 kNm." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1891m. The activity was categorized as 'drilling -- ream' and lasted for 3.5 hours. Operational details: Circulated hole clean, reciprocated string from 2021m to 2035m. 4500 l/min, 265 bar, 150 rpm, 12-14 kNm. Lots of cuttings on shakers after 1 x bottom up. Circulated 4 x bottom up in total." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1891m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pumped out from 2021m to 1891m. 2500 l/min, 91 bar." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1891m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Attempted to POOH from 1891m without pumping. Took 20 tom over pull at 1889m." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1449m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Pumped out from 1891m to 1449m. 4500 l/min, 250 bar." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1367m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Reduced flow to 2000 l/min, 54 bar while pulling Power Drive into shoe and 1 stand into 20' casing to 1367m.." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1367m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated 2 x bottom up at shoe, 4000 l/min, 175 bar." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1367m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flow checked well, 400 l/hr static loss. Simultaneously, checked and greased PRS." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1367m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pumped and displaced 4,7m3 1,75 sg slug." "On 2009-04-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 774m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: POOH from 1367m to 774m." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' BHA from 774m to 196m." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flow checked well prior to pull BHA through BOP. Meanwhile removed PS 21 slips and installed master bushing." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Operated BOP rams and annular." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Tool Box Talk prior to pull and rack BHA." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 85m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pulled and racked 17 1/2 ' BHA from 196m to 85m and racked on set back." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 85m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: Stop due to malfunction on fingers on finger board in derrick. Trouble shot." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 17 1/2' BHA from 85m to surface. B/O x-overs and layed down. Downloaded ARC tool as pr Schlumberger procedure. Racked 9 1/2' stand on set back." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleared and cleaned rigfloor." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to pick up wear bushing pulling tool and stand with jetsub." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked 1 stand of 5 1/2' HWDP and connected jet sub. RIH and jetted BOP." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up and run wear bushing pulling tool on top of 1 stand 5 1/2' HWDP with jetting sub." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to RIH and retrieve wear bushing." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH from 40m to 138m. Dropped 2 3/4' drift." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Jetted wear bushing prior to retrieving same. 2400 l/min, 40 bar, 2 rpm." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Latched on wear bushing. Took 8 ton over pull and pulled free. Measured from tooljoint to land off point, 8,70m." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with wear bushing from 138m to surface." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: L/D wear bushing and 4 joints of HWDP. Retrieved drift." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Cleared and cleaned rigfloor." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Lowered work platform and piston TDS." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to change washpipe." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Changed washpipe on DDM. Leakage tested same to 240 bar, OK." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to rig up for running 13 3/8' casing." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Rigged up 13 3/8' casing handling equipment." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to run 13 3/8' casing." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 13m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: P/U 13 3/8' casing shoe joint with reamer shoe and checked for flow through with water. Installed bypass baffle." "On 2009-04-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 290m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Ran 13 3/8' casing as per tally from 13m to 290m." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 794m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Ran 13 3/8' casing as per tally from 290m to 794m. Max running speed 10 joints per hour." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1310m. The activity was categorized as 'drilling -- casing' and lasted for 6.5 hours. Operational details: RIH with 13 3/8' casing from 794 - 1315 m; held pre-job safety meeting with day crew, filled casing with 1.51 sg OBM every 5 joints." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1310m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: R/U and function tested Tesco CDS tool; held pre-job safety meeting with involved personnel prior to operations." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1310m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and tidied up rig floor." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1382m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with stands of 13 3/8' casing from 1310 - 1382 m; held pre-job safety meeting with involved personnel prior to operations, filled casing with 1.51 sg OBM as RIH." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1382m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke circulation and circulated casing with 1.51 sg OBM prior to running into open hole (1100 lpm, 13 bar)." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1382m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U new stand of 13 3/8' casing from derrick, unable to operate forward PRS." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1382m. The activity was categorized as 'interruption -- maintain' and lasted for 2.8 hours. Operational details: Troubleshot PRS lower arm; replaced drilling control software." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1382m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed toolbox talks with new crew; went through Tesco CDS tool operations." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1382m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Continued to troubleshot forward PRS; unable to lift upper arm." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1418m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with stands of 13 3/8' casing from 1382 - 1484 m; broke out and dressed threads on Tesco CDS tool due to alignement problems." "On 2009-05-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1848m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with stands of 13 3/8' casing from 1418 - 1848 m; filled casing with 1.51 sg OBM as RIH." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2195m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with stands of 13 3/8' casing from 1848 - 2195 m while simultaneously filling casing with 1.51 sg OBM, lost max 15 tons weight . Attempted to pass through obstruction at 2195 m, no-go." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2210m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke circulation and gradually increased pump rate to 1000 lpm / 18 bar. Carefully washed down casing stand to 2210 m. Attempted to RIH with next casing stand without circulation; imediately lost weight." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2235m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Washed down with 13 3/8' casing from 2210 - 2235 m (1500 lpm, 22 bar); lost max 15 tons weight, unable to pass through obstruction. Gradually increased pump rate from 1500 - 2000 lpm / 22 - 35 bar." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2235m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Circulated 13 3/8' casing at 2000 lpm / 37 bar; had to restart circulation twice due to pack-off, max SPP 75 bar." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2290m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Washed / reamed 13 3/8' casing down from 2235 - 2290 m; 2000 lpm, 16 - 35 bar, 1 rpm, 20 - 25 kNm. Observed increasing drag, packed off casing string at 2290 m." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2290m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Shut down pumps, worked casing string and re-established circulation. Gradually increased pump rate to 2500 lpm / 23 bar." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2354m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Washed / reamed 13 3/8' casing down from 2290 - 2354 m (2500 lpm, 22 - 35 bar, 1 rpm, 20 - 25 kNm); set down max 15 tons on casing." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2356m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Established circulation after connection, worked casing down from 2354 - 2356 m; 2500 lpm, 22 - 35 bar, 1 rpm, 20 - 25 kNm. Packed off casing string at 2356 m." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2354m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Shut down pumps, worked casing string and gradually increased pump rate (2200 lpm, max SPP 40 bar, 1 rpm, max 25 kNm); packed off several times and finally lost returns." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2354m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Worked casing string and attempted to re-establish circulation, no-go." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2354m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out wet and racked back 13 3/8' casing stand in derrick; held pre-job safety meeting with involved personnel prior to operation. Broke casing coupling on box end; had to adjust Weatherford tong back-up jaws accordingly to prevent unscrewing coupling." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2354m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: POOH 5 m and verified casing string free. Gradually increased pump rate to 2500 lpm / 23 bar. Circulated BU while reciprocated casing string from 2354 - 2348 m; observed clean returns over shakers. M/U next casing stand." "On 2009-05-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2357m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke circulation and gradually increased pump rate. Washed 13 3/8' casing down from 2354 - 2357 m; 2500 lpm, 23 bar." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2462m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Washed 13 3/8' casing down from 2357 - 2462 m; 2500 lpm, 23 - 25 bar." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2462m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated 13 3/8' casing at 2500 lpm / 23 bar. Meanwhile held pre-job safety meeting with involved personnel prior to R/D Tesco tool and M/U casing hanger." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2462m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: R/D Tesco CDS tool and changed to 5 1/2' DP handling equipment." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2462m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: M/U 13 3/8' casing hanger assy." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2462m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Removed FMS and installed master bushing. Meanwhile established circulation at 2000 lpm / 21 bar." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2471m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Washed down with 13 3/8' casing from 2462 - 2471 m at 2000 lpm / 21 bar." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2471m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: R/D casing tong." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2603m. The activity was categorized as 'drilling -- casing' and lasted for 7.5 hours. Operational details: M/U first stand of 5 1/2' HWDP. Broke circulation and gradually increased pump rate to 2430 lpm / 34 - 46 bar. Washed down with 13 3/8' casing from 2471 - 2603 m on 5 1/2' HWDP landing string." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2603m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: M/U cementing head." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Broke circulation and gradually increased pump rate to 2200 lpm / 44 bar. Washed down with 13 3/8' casing from 2603 - 2607.5 m, landed hanger and set down casing weight + 8 tons." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Circulated and conditioned mud prior to casing cementing job; broke circulation and gradually increased pump rate to 2960 lpm / 64 bar, circulated a total of 1.2 x casing volumes. Mud weights in/out = 1.51 sg, no losses seen. Meanwhile held pre-job safety meeting with involved personnel prior to cementing operations; reviewed check lists and relevant safety / operational issues." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped 8 m3 of base oil, followed by 20 m3 of 1.60 sg Tuned spacer E+ with rig pumps at 1200 - 1550 lpm. Displaced spacer to rig floor with 3 m3 of 1.51 sg OBM. Lined up to pump from cement unit, verified surface routing - OK." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Released bottom dart. Mixed and pumped 28 m3 of 1.90 sg cement slurry with cement unit at 800 - 900 lpm. Displaced surface cementing lines with 0.5 m3 drill water, released top dart. Flushed surface cementing lines with additional 1.5 m3 drill water. Lined up to pump 1.51 sg OBM with rig pumps." "On 2009-05-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Started to displace cement slurry in place with rig pumps at 2960 lpm / 47 bar. Unable to verify bottom wiper plug land / shear." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued to displace cement slurry in place with rig pumps; recorded 20 bar pressure increase when cement spacer / slurry entered into open hole. Reduced pump rate to 1200 lpm / 27 bar prior to bumping top plug. No losses seen during the entire cementing and displacement operations. Bumped top wiper plug at 8704 strokes, corresponding to 96.2 % pump efficiency. Shut down pumps and observed pressure drop from 38 - 18 bar. Pumped additional 20 strokes and observed pressure increase from 18 - 31 bar with returns back to surface. Shut down pumps." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Bled off casing pressure; 0.4 m3 OBM in return, verified float - OK." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Installed seal assembly according to Vetco procedure; held pre-job safety meeting with involved personnel prior to operations." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Leak tested seal assembly to 35/300 bar for 5/15 min - OK." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released PADRT and L/D cementing head." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and tidied up rig floor." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed 2 x sponge balls, wiped / flushed 5 1/2' HWDP landing string at 660 lpm / 4 bar." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Retrieved casing landing string, L/D PADRT and 2 x 5 1/2' HWDP joints. Held pre-job safety meeting with involved personnel prior to operations." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: R/D top drive air hose for Tesco CDS tool, removed excess casing handling equipment from rig floor." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: RIH with jet sub and WB assy, cleaned WH area at 1500 lpm / 10 bar." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Installed 13 3/8' wear bushing; over-pull tested same 4 tons - OK. POOH and L/D WBRT." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: M/U and RIH with BOP test tool; held pre-job safety meeting with involved personnel prior to operations." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 48m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.5 hours. Operational details: Leak tested BOP and TDS IBOP`s to 20/345 bar for 5/10 min - OK." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: POOH with BOP test assy, L/D test tool, XO`s and jet sub." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleaned and tidied up rig floor. Meanwhile inspected / greased top drive." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.8 hours. Operational details: Cut and slipped drilling line; held pre-job safety meeting with involved personnel prior to operations. Calibrated crown and floor savers." "On 2009-05-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: L/D 17 1/2' drilling BHA from derrick; inspected PRS dies / rollers and held pre-job safety meeting with involved personnel prior to operations." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Continued to L/D 17 1/2' drilling BHA from derrick." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned and tidied up rig floor. Meanwhile prepared to P/U 12 1/4' BHA." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Started to M/U 12 1/4' BHA; held pre-job safety meeting with involved personnel prior to operations. Meanwhile prepared for casing test." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Leak tested surface lines to 35/300 bar for 5/10 min - OK. Meanwhile lifted BHA out of hole." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Attempted to leak test 13 3/8' casing against shear rams with 1.51 sg OBM; pressure dropped at 90 bar and stabilised at 67 bar, 1250 ltr pumped when shutting down pump." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Bled off casing pressure, evaluated further operations." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Deactivated Schlumberger ARC tool, racked 12 1/4' BHA stand in derrick." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: P/U 3 x 8 1/4' DC`s from deck, M/U and racked stand in derrick; held pre-job safety meeting with involved personnel prior to operations." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Held pre-job safety meeting with involved personnel prior to P/U 5 1/2' DP from deck. Moved rollers and changed to 5 1/2' DP handling equipment." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 795m. The activity was categorized as 'drilling -- trip' and lasted for 4.8 hours. Operational details: M/U and RIH with 5 1/2' DP to 795 m; P/U single joints from deck." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 5 1/2' DP, racked same in derrick." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Leak tested 13 3/8' casing with 1.51 sg OBM to 55 bar, pumped 746 ltr, bled back 720 ltr - OK; held pre-job safety meeting with involved personnel prior to operations." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held pre-job safety meeting with involved personnel prior to M/U 12 1/4' BHA, cleaned and tidied up rig floor." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: M/U and RIH with 12 1/4' BHA; initialized Schlumberger ARC tool." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: RIH with BHA on 5 1/2' DP from 178 - 600 m; filled pipe every 300 m." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Function tested Schlumberger tools at 2300 lpm / 95 bar - OK." "On 2009-05-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1550m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RIH with BHA on 5 1/2' DP from 600 - 1550 m; filled pipe every 300 m, performed kick drill with crew." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RIH with BHA on 5 1/2' DP from 1550 - 2562 m; filled pipe every 300 m." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Broke circulation and gradually increased pump rate to 2300 lpm / 149 bar. Took up / down / free rotating torq = 167 / 133 / 148 tons, free rotating torq 13 - 16 kNm at 20 rpm. Meanwhile held pre-job safety meeting with involved personnel prior to mud displacement operations." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2577m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Washed down with BHA from 2562 m, tagged float at 2577 m." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2578m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled cement wiper plugs and casing float from 2577 - 2578 m; 2780 lpm, 204 - 158 bar, 40 - 70 rpm, 14 - 17 kNm, 1 - 3 tons WOB. No indications of hard cement. Meanwhile displaced well to 1.30 sg OBM." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2599m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 13 3/8' casing shoe track from 2578 - 2599 m; 2780 lpm, 154 - 158 bar, 70 rpm, 14 - 16 kNm, 0 - 3 tons WOB. No indications of hard cement." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2599m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Displaced kill / choke lines to 1.30 sg OBM." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2607m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 13 3/8' casing shoe / shoe track from 2599 - 2607 m (2780 lpm, 153 - 156 bar, 50 - 70 rpm, 13 - 19 kNm, 1 - 7 tons WOB); hard drilling from 2604 m." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Reamed / cleaned out rat hole from 2607 - 2616 m; 2780 lpm, 147 - 150 bar, 100 rpm, 13 - 16 kNm, 0 - 0.5 tons WOB." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2619m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 12 1/4' hole from 2616 - 2619 m; 2780 lpm, 148 bar, 100 rpm, 16 - 18 kNm, 5 tons WOB." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2599m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated and conditioned mud BU while reciprocating pipe (2780 lpm, 149 bar, 0 - 100 rpm, 0 - 16 kNm); MW in/out = 1.30 sg, clean returns over shakers. Pulled BHA above 13 3/8' casing shoe." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2599m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: Performed FIT to 1.4 sg EMW, pumping down pipe and annulus simultaneously; max 26 bar, pumped 361 ltr and bled back 330 ltr during test." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2618m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Washed / reamed down to 2618 m, took SCR`s. Monitored up / down / free rotating torq = 170 / 139 / 153 tons, free rotating torq 13 kNm / 20 rpm. Established drilling parameters; monitored ESD from ARC tool = 1.422 sg EMW." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2719m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled 12 1/4' hole from 2619 - 2719 m; 3500 lpm, 216 - 220 bar, WOB 5 - 8 tons, 170 rpm, 17 - 21 kNm, ECD 1.31 - 1.33 sg EMW, ESD 1.30 - 1.32 sg EMW, ROP 30 m/hr." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2719m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Shut down rig power for generator maintenance." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2758m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 12 1/4' hole from 2719 - 2758 m; 3500 lpm, 217 - 222 bar, WOB 5 - 8 tons, 170 rpm, 18 - 20 kNm, ECD 1.32 - 1.34 sg EMW, ESD 1.31 - 1.32 sg EMW, ROP 26 - 28 m/hr. Mud pumps shut down. Meanwhile PU and racked 9 5/8' stands in derrick." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2758m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Troubleshot mud pumps; cleared filter for cooling of switchboard, resat electrical breaker switch. Meanwhile PU and racked 9 5/8' stands in derrick." "On 2009-05-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 12 1/4' hole from 2758 - 2770 m; 3500 lpm, 217 - 222 bar, WOB 5 - 8 tons, 170 rpm, 18 - 20 kNm, ECD 1.33 - 1.34 sg EMW, ESD 1.31 - 1.32 sg EMW, ROP 26 - 30 m/hr. Meanwhile PU and racked 9 5/8' stands in derrick." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2825m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' hole from 2770 - 2825 m; 3500 lpm, 221 - 223 bar, WOB 5 - 8 tons, 170 rpm, 18 - 23 kNm, ECD 1.33 - 1.34 sg EMW, ESD 1.31 - 1.32 sg EMW, ROP 30 - 32 m/hr. Unable to obtain directional control with Xceed tool. Meanwhile PU and racked 9 5/8' stands in derrick." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2820m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Picked off bottom and troubleshot Xceed tool; unable to obtain tool response on downlink commands, decided to POOH. Meanwhile PU and racked 9 5/8' stands in derrick." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2825m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Circulated hole clean with 2 x BU; 3500 lpm, 223 bar, 80 - 130 rpm, 14 - 15 kNm. Meanwhile completeted PU and racking 9 5/8' stands in derrick. 9 stands made up totally. Status: 24 stands of 9 5/8' casing in derrick." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2800m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Set back last stand in derrick. Flow checked well on trip tank - OK." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2680m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH wet with 12 1/4' BHA from 2825 - 2680 m." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH wet to the shoe with 12 1/4' BHA from 2680 m to 2595 m." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Flowchecked well inside shoe at 2595 m. Lossrate 180 l/ hr. Meanwhile held TBT prior to POOH, checked PRS dies." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 5 m3 1,55 sg slug and filled trip tank. Removed mud bucket. Observed problem with drawwork motor." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Investigated problem with drawwork. Kept hard tripping in both directions." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: POOH with 12 1/4' BHA from 2598 m to 178 m. Slower pulling speed to 2196 m due to problem with drawwork. Rectified problem and de-assign motor #4." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well prior to POOH with BHA, static. Meanwhile held TBT and removed PS-21 slips." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 12 1/4' BHA from 178 m to surface. B/O 12 1/4' bit and L/D Xceed tool." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 19m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: TBT prior to P/U new Xceed tool. P/U new Xceed tool and M/U 12 1/4' bit. RIH from surface to 19 m." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Downloaded data from telescope and Arc tools as per Schlumberger instructions." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 179m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA from 19 m to 179 m." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 179m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 620m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 179 m to 620 m." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 620m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Filled pipe and shallow tested MWD tools with 2300 lpm/ 78 bar." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 620 m to 2595 m. Filled pipe every 600 m." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Serviced TDS. Observed problem with Drawwork motors." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Investigated problem with drawwork motors. Rectified problem and de-assign motor # 2." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2761m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 2595 m to 2761 m." "On 2009-05-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2780m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Reamed and washed down from 2761 m to 2780 m. Parameters; 3000 lpm/ 182 bar - 60 rpm/ 13 kNm." "On 2009-05-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2825m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Reamed and washed down from 2780 m to 2825 m, whilst setting toolface. Parameters; 3000 lpm/ 182 bar - 60 rpm/ 13 kNm." "On 2009-05-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2902m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled 12 1/4' hole from 2825 to 2902 m; 3500 lpm, 228 - 230 bar, WOB 6 - 14 tons, 170 rpm, 18 - 24 kNm, ECD 1.33 - 1.34 sg. ROP 25 m/hr. Note: Hard formation from 2889 m to 2892 m. Started adding LCM mud into active when started drilling." "On 2009-05-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3212m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 12 1/4' hole from 2902 to 3212 m; 3500 lpm, 225 - 230 bar, WOB 5 - 8 tons, 170 rpm, 18 - 25 kNm, ECD 1.34 - 1.36 sg. ROP 20-40 m/hr Note: Hard stringers from 3013 m to 3022 m, 3153 m to 3156 m. Used different RPM and WOB parameters while drilling stringers. ROP in stringers: 2-5 m/hrs" "On 2009-05-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3280m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole from 3212 m to 3280 m; 3500 lpm, 227 - 230 bar, WOB 6 - 14 tons, 170 rpm, 18 - 30 kNm, ECD 1.34 - 1.35 sg. ROP 30-40 m/hr Note: Hard stringers from 3227 m to 3229 m, 3262 m to 3280 m. Used different RPM and WOB parameters while drilling stringers. ROP in stringers: 2-5 m/ hrs." "On 2009-05-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3309m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 12 1/4' hole from 3280 m to 3309 m; 3500 lpm, 221 - 222 bar, WOB 8 - 14 tons, 120 - 190 rpm, 18 - 30 kNm, ECD 1.33 - 1.34 sg. ROP 1- 4 m/hr Note: Top Shetland and hard formation from 3266 m. Attempted to optimise ROP by using different RPM and WOB parameters." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3315m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole from 3309 m to 3315 m; 3500 lpm, 219 - 222 bar, WOB 12 - 15 tons, 120 - 190 rpm, 18 - 26 kNm, ECD 1.33 - 1.34 sg. ROP 0,5 - 2 m/hr Note: Top Shetland and hard formation from 3266 m. Attempted to optimise ROP by using different RPM and WOB parameters." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3319m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: Drilled 12 1/4' hole from 3315 m to 3319 m; 3500 lpm, 217 - 219 bar, WOB 12 - 15 tons, 120 - 190 rpm, 19 - 28 kNm, ECD 1.33 - 1.34 sg. ROP 0,5 - 1 m/hr. Had minor progress in ROP last 2 hours, and decided to POOH. Note: Top Shetland and hard formation from 3266 m. Attempted to optimise ROP by using different RPM and WOB parameters." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3319m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well prior to POOH. Observed loss of 70 l/ 30 min." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3083m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH wet with 12 1/4' BHA from 3319 m to 3083 m. Recorded up/ down weight prior to POOH; 185 ton/ 133 ton." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3083m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 5 m3 1,60 sg slug. Meanwhile checked PRS dies." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2889m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 3083 m to 2889 m. Took weight at 2889 m, max OP 30 ton. Note: 2889 m, limestone stringer at transition zone Heimdal/ Lista formations." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2850m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Reamed tight area at 2889 m with no pump. String torqued up to 40 kNm/ 30 rpm. Established circulation with 500 lpm/ 39 bar. Increased flowrate stepwise to 3500 lpm/ 225 bar - 15 rpm/ 13 kNm. Pumped out from 2889 m to 2875 m." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH wet with 12 1/4' BHA from 2875 m to 2595 m inside 13 3/8' shoe. No obstruction in rest of OH and shoe area." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well inside shoe, static. Meanwhile performed service on TDS and aft PRS." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 5 m3 1,60 sg slug." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Continued servicing TDS, PRS and drawwork." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 192m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 2595 m to 192 m." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 192m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed PS-21 slips and installed master bushing. Performed kick drill with involved personnel." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 192m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well prior to POOH with BHA. Meanwhile repaired loose connection on drawwork motor # 2." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 192m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Continued to repair loose connection on drawwork motor # 2. Meanwhile observed well on trip tank." "On 2009-05-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 12 1/4' BHA from 192 m to 100 m." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 12 1/4' BHA from 100 m to surface. Racked same in derrick." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Gauged and inspected bit and BHA. Upper stabilizer had 1/32'' wear. In addition it was ringed out with a 4cm high and 2-3mm deep cut all around the stab approximately 1/3 from the bottom of it. The hard facing was still in place. The lower stab was worn 1/16''. Also here the hard facing was in place. Bit grading: 2-2-WT-S-IN-HC, some wear also on bit body. B/O bit and M/U new 12 1/4' bit." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: RIH with 12 1/4' BHA from surface to 178 m." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed master bushing and installed PS-21 slips." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1992m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 178 m to 1992 m. Filled pipe every 600 m." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 1992 m to 2598 m. Filled pipe every 600 m." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Function test BOP rams. Flushed kill and choke lines inside shoe at 2598 m. Recorded up and down weight prior to RIH to OH; 170 ton/ 135 ton." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2854m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 2598 m to 2854 m. Took weight at 2854 m, 20 ton down weight." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2850m. The activity was categorized as 'drilling -- ream' and lasted for 1.8 hours. Operational details: Washed/ reamed down from 2854 m to 2882 with 1000 lpm/ 25 bar - 50 RPM/ 14-23 kNm. Worked tight spots. Increased pumprate to 2900 lpm/ 166 bar. Backreamed stand to 2857 m and observed a pressure peak to 195 bar and packed off the hole. Resiprocated string and attempted to stage up flowrate slowly with 10 SPM, no return seen. Dry reamed out from 2857 m to 2850 m. Lost 2,5 m3 to formation." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2850m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Monitored well on triptank. Initial loss rate 12 m3/ hr and decreased to 1,1 m3/ hr. Total loss 8.2 m3." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2850m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Pumped and displaced 11 m3 LCM pill at 2850 m with 780 lpm/ 20 bar. Lost 6,5 m3 to formation while pumping LCM pill." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2850m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well on triptank. Observed losses 400 l/ hr static losses." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2676m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 2850 m to 2676 m." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2676m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Established circulation at 2676 m. Increased flowrate slowly to 3500 lpm/ 220 bar, observed no loss to formation." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2889m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 2676 m to 2889 m. Took 20 ton down weight at 2889 m." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2900m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Reamed without pumping from 2889 m to 2900 m with 30 RPM. String torqued up and took weight." "On 2009-05-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2995m. The activity was categorized as 'drilling -- ream' and lasted for 7.5 hours. Operational details: Washed and reamed in hole from 2900 m to 2995 m. Parameters: 3500 lpm/ 224 bar. 30-60 RPM/ 20-25 kNm. Max torque 40 kNm. Staged pumps up slowly after each connection. Had several areas through claystone stringers with packing off tendency. Max standpipe pressure observed 230 bar. Claystone stringer from 2932 m to 2936 m, 2971 m to 2973 m." "On 2009-05-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3025m. The activity was categorized as 'drilling -- ream' and lasted for 3.0 hours. Operational details: Washed and reamed in hole from 2995 m to 3025 m. Parameters: 3500 lpm/ 224 bar. 30-60 RPM/ 20-25 kNm. Max torque 40 kNm. Staged pumps up slowly after each connection. Had several areas through claystone stringers with packing off tendency. Max standpipe pressure observed 230 bar. Claystone stringer from 2999 m to 3001 m and from 3009 m to 3011 m." "On 2009-05-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3139m. The activity was categorized as 'drilling -- ream' and lasted for 3.0 hours. Operational details: Observed better hole condition from 3025 m. Washed and reamed in hole from 3025 m to 3139 m. Parameters: 3500 lpm/ 223 -225 bar, 50 RPM/ 14-21 kNm. Attempted to wash down without rotation at 3123 m, no go." "On 2009-05-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3319m. The activity was categorized as 'drilling -- ream' and lasted for 5.0 hours. Operational details: Washed and reamed in hole from 3129 mMD to 3319 mMD and tagged bottom. Parameters: 3500 lpm/ 223 -225 bar, 60 RPM/ 16-23 kNm." "On 2009-05-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3319m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed SCR readings at 3319 mMD/ 2642 mTVD with MW 1,30 sg. MP#2: 20 SPM/10 Bar - 30 SPM/ 14 Bar - 40 SPM/ 20 bar. MP#3: 20 SPM/ 9 Bar - 30 SPM/ 14 Bar - 40 SPM/ 20 Bar." "On 2009-05-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- drill' and lasted for 12.8 hours. Operational details: Established drilling parameters and drilled 12 1/4' hole from 3319 m to 3422 m. Parameters: 3500 lpm/ 228 - 230 bar, 170 RPM/ 21-25 kNm, WOB: 7-13 ton, ROP: 5-13 m/hr, ECD: 1,34-1,35 sg." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3433m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 12 1/4' hole from 3422 m to 3433 m. Parameters: 3500 lpm/ 225-232 bar, 170 RPM/ 21-30 kNm, WOB: 7-13 ton, ROP: 8-13 m/hr, ECD: 1,33-1,34 sg. Note: Hard stringer at 3422 m and from 3428 m to 3433 m. ROP at stringer 1-3 m/hr." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3437m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Continued drilling 12 1/4' hole from 3433 m to 3437 m. Parameters: 3500 lpm/ 229 bar, 170 - 190 RPM/ 17-22 kNm, WOB: 4-10 ton, ROP: 1-3 m/hr, ECD: 1,33 sg. Observed problem with mudpumps. Note: Hard formation from 3433 m to 3437 m." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3437m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Troubleshot problems with mud pumps #1 and #2. Repaired liner spray." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drilling 12 1/4' hole from 3437 m to 3442 m, TD of section. Parameters: 3500 lpm/ 229 bar, 170 - 190 RPM/ 17-22 kNm, WOB: 4-10 ton, ROP: 1-4 m/hr, ECD: 1,33 sg. Observed softer formation from 3339 m and increased ROP from 1 m/hr to 4 m/hr. Note: Hard formation from 3437 m to 3439 m." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Took survey at 3442 mMD, TD of section. Survey depth: 3426,62 mMD/ 2652,73 mTVD. Inc 85,4dgr - Az 121,89 dgr. Compared to plan: 3,8 m left/ 1,0 m high." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated hole clean while resiprocated string at 3342 m. Parameters: 3500 lpm/ 235 bar, 80 RPM up and 160 RPM down/ 15-19 kNm." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well on trip tank - static." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took up/ down WT and torque readings at 3432 m: 185 ton up/ 127 ton down. Torque: 22 kNm/ 10 RPM and 152 ton rot. WT." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3243m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH wet with 12 1/4' BHA on 5 1/2' DP from 3442 m to 3243 m." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3243m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well on trip tank, had initial losses 480 l/hr, but decreasing trend to 360 l/hr." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3243m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Dropped 3' drift for 5 1/2' DP. Pumped same down with 2000 lpm/ 87 bar and landed off with 136 bar." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3243m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped and chased 5 m3 1,56 sg slug." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2907m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 3243 m to 2907 m. Encountered tight spot at 2907 m, max OP 20 ton." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2907m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Attempted to rotate through tight spot at 2907 m, no go. Attempted to ream through with 500 lpm/ 10 bar, 20 RPM/ 14-30 kNm, no go. Observed signs of packing off." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2880m. The activity was categorized as 'drilling -- ream' and lasted for 1.2 hours. Operational details: Run in hole to 2920 m. Attempted to stage pumps up to 3500 lpm, no go. Observed 204 bar with 2500 lpm, previously had 136 bar with 2500 lpm. Probable due to drift in string. Reamed out of hole from 2920 m to 2880 m with 2750 lpm/ 244 bar, 30 RPM/ 15-18 kNm." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2840m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: Attempted to pull on elevator from 2880 m, no go. Encountered tight spot at 2872 m, max OP 25 ton. Run in hole to 2880 m and M/U TDS. Attempted to rotate through tight spot at 2872 m, no go. Attempted to ream through with 500 lpm/ 18 bar, 20 RPM/ 14-30 kNm, no go. Reamed out of hole from 2880 m to 2840 m with 2750 lpm/ 245 bar, 30 RPM/ 15-25 kNm." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH wet with 12 1/4' BHA on 5 1/2' DP from 2840 m to 2598 m and into the 13 3/8' shoe. No restriction observed in rest of OH or shoe area." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well on trip tank, static." "On 2009-05-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took up/ down WT and torque readings at 2598 m: 172 ton up/ 136 ton down. Torque: 11-13 kNm/ 10 RPM, 10-14 kNm/ 20 RPM and 154 ton rot. WT." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped and chased 5 m3 1,6 sg slug." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Monitored well on trip tank while repairing ESD system on rig. Initial losses 100 l/hr." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Serviced PRS and TDS." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 2598 m to 178 m." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Flowchecked well on triptank prior to POOH with BHA, had initial losses 200 l/hr. Meanwhile removed PS-21 slips and installed master bushing. Rearranged pipe in derrick." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'interruption -- rig up/down' and lasted for 2.8 hours. Operational details: When rearranged drill collar stand in derrick, drill collar stand went stuck in the fingerboard. Troubleshot on same and sorted out the problem. Removed the stand." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: TBT prior to POOH with BHA with focus on manual handling, working in red zones and hand injuries." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: POOH with 12 1/4' BHA from 178 m to surface. Racked HWDP and DC in derrick. Laid out remaining BHA components." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Inspected TDS for loose items, cleaned and cleared rig floor." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: TBT prior to R/U for running 9 5/8' liner with focus on heavy lifts, pinch points and hand injuries." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: R/U to run 9 5/8' liner. Meanwhile pressure tested CRI hose to 200 bar/ 10 min." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: TBT prior to run 9 5/8' liner with focus on falling objects, barriers, red zones and M/U torque." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 911m. The activity was categorized as 'drilling -- casing' and lasted for 6.5 hours. Operational details: RIH with 9 5/8' liner from surface to 923 m. Floats tested in shoe joint. Filled every stand. Checked PRS and slip dies every 10 stands. Running speed: 142 m/ hr." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 911m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Hold tool box meeting with crew prior to P/U hanger." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 911m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed auto slips and installed master bushing." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 923m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 9 5/8' liner from 911 m to 923 m. Changed BX elevator to 6 5/8' elevators." "On 2009-05-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 923m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U 9 5/8' hanger assy. Run MX ball seat assy into 9 5/8' liner. Land off on C plate. M/U MX assy to running tool." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 923m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Performed pull test of hanger assy and running tool. Filled PBR with hi vis pill. Liner weight 55 ton." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 940m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran hanger assy through rotary. R/D casing tong and manual elevators." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 940m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: M/U x-over and pup to running tool." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 940m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed out elevators and installed elevator rotator." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 940m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up DP stand to pup. Installed auto slips." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1867m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 9 5/8' liner on 5 1/2' DP from 940 m to 1867 m. Filled every 5 stands. Running speed 412 m/ hr. Total losses while RIH with 9 5/8' liner from surface to 1867 m; 7,6 m3. Losstrend is decreasing." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 9 5/8' liner on 5 1/2' DP from 1867 m to 2595 m. Filled every 5 stands. Running speed 364 m/ hr. Took up and down weight inside shoe at 2595 m, 185 ton/ 138 ton." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: At 2595 m broke circulation and increased flowrate stepwise to 2000 lpm/ 46 bar. Meanwhile serviced Iron roughneck." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2595m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired hydraulic leak on aft iron roughneck. Meanwhile continued circulated with 1500 lpm/ 31 bar. Total pumped in shoe: 88 m3." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2863m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 9 5/8 liner on 5 1/2' DP from 2595 m to 2863 m. Took weight at 2863 m, max down weight 40 ton." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2865m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Attempted to wash through tight spot at 2863 m, no go.Parameters: 500 - 750 lpm/ 20 bar. Washed/ rotated liner down from 2863 m to 2865 m. Parameters: 1000 lpm/ 21 bar - 15 RPM/ 15-30 kNm." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3401m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 9 5/8' liner on 5 1/2' DP from 2865 m to 3401 m." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Washed down last stand from 3401 m to 3440 m with 400 lpm/ 17 bar. Recorded up and down weight at setting depth; 195 ton/ 134 ton." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U and M/U cement head." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Washed in hole to TD at 3442 m with 400 lpm. Set down 10 ton. Pulled out to up weight and additional 2 m to 3439 m. Estimated loss of 14 m3, while RIH with 9 5/8' liner from surface to TD." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Circulated at setting depth of the liner at 3439 m. Increased flowrate stepwise to 1200 lpm/ 35 bar, and loss free rate. Total pumped 100 m3, one OH volume." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Dropped ball from the cement head and chased the ball down with 500 lpm/ 14 bar. Ball landed in ball seat with 166 bar and after pumped 13,5 m3. Verified hanger set by slacking off to 30 ton down weight. Bleed off pressure. Pulled up and left 10 ton weight on RT." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released running tool with 11 turns clockwise. P/U to free weight and 1 additional meter to check that running tool was free and activated MX ball seat. Slacked off 20 ton to shear out ball seat." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Staged up pumps to 2000 lpm/ 63 bar without losses." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Reduced flowrate to 500 lpm, 16 bar. Established rotation 20 RPM/ 19-23 kNm. Increased flowrate to 2000 lpm/ 65 bar. Circulated BU with loss free circulation. Meanwhile held TBT with focus on cement job." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 15 m3 0,83 sg base oil with rig pump." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped 20 m3 1,3 sg Spacer with rig pump. Chased spacer with 3 m3 OBM, which meant 1,5 m3 spacer behind cement." "On 2009-05-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Dropped lower SSR dart for bottom wiper plug. Confirmed same with flag." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Mixed and pumped 38 m3 1,90 sg cement slurry with 800 lpm/ 49-36 bar, 20 RPM/ 17-30 kNm. Displaced cement to rig floor with 890 liter fresh water. Dropped upper SSR dart for top wiper plug. Confirmed same with flag." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Displaced cement with OBM. Pumped with 2000 lpm - 20 rpm/ 28-42 kNm. Observed top dart at wiper plug at 1290 strokes, calculated stroke with 96 % efficiency were 1227 stroke. Top dart sheared out at 216 bar. No bump observed after 2770 strokes. Pumped totally 60,7 m3. Total losses during cement job 8,5 m3. Unable to rotate string after 2000 strokes displaced volume. Bleed off and checked for back flow, none observed." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3439m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Set TSP packer according to Weatherford prosedure. Closed annular, and pressure up annulus to 200 bar for 5 min and tested TSP packer." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressured up to 25 bar. Released RSM by pulling out 16 m with running tool." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Circulated out excess cement with 3000 lpm/ 90 bar. Observed spacer but no cement in return." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: B/O cement head. Observed backflow from string. Reinstalled cement head on string." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued circulating to prevent backflow 3000 lpm/ 91 bar." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Circulated and conditioned mud with RT inside PBR at 2508 m. 3000 lpm/ 90 bar. Observed for backflow, none." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: B/O cement head and single and loaded sponge balls." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped down sponge balls to clean DP with 3000 lpm/ 90 bar." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Flow checked well, static." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 5 m3 1,60 sg slug, chased with OBM." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2461m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: L/D cement head with one single on catwalk, disconnected hoses on same. POOH and racked back one stand with 5 1/2' DP. P/U cement head and 1single from catwalk. RIH with single DP, B/O and L/D cement head." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH with liner hanger RT on 5 1/2' DP from 2461 m to 38 m. (1212 m/ hr.)" "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed master bushing." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with liner hanger RT from 38 m to surface. L/D liner hanger RT." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held TBT prior to RIH with jet sub and test plug." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: RIH with jetsub and 1 std 5 1/2' DP. MU testplug on top of stand and RIH to 139 m. Jetted wearbushing and landed off test plug at 139 m, jetsub depth 180 m." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: Attempted to pressure test 18 3/4' BOP, no go. Had leakage at cement unit. Greased up valves at cement unit." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.8 hours. Operational details: Pressure tested 18 3/4 BOP to 30 bar/ 5 min - 345 bar/ 10 min. Meanwhile drifted DP in derrick." "On 2009-05-16, at Well NO 15/9-F-10, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with jetsub/ testplug from 180 m to 100 m." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH with testplug assy from 100 m to surface. L/D testplug and jetsub." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held TBT prior to test 9 5/8' liner. Attempted to test 9 5/8' liner to 300 bar, no go. Pressured up to 240 bar. Pressure seemed to start leaking at 180 bar. After pressured up to 240 bar, pressure dropped to 231 bar in 2 min. Bleed off pressure. Meanwhile continued drifting DP in derrick and preparing 8 1/2' BHA." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Continued WOC for testing of liner. Meanwhile changed washpipe and saversub on TDS. Leak tested washpipe to 200 bar." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Continued WOC for pressure testing entire well. Meanwhile changed saversub on TDS. Rearranged fingerboard and M/U jar and accelerator on 5' HWDP. Racked same in derrick." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held TBT prior to pressure test of 9 5/8' liner. Confirmed line up and flushed lines." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Attempted to pressure test entire well to 300 bar, no go. Pressured up to 250 bar. Observed a steady leakrate of 5 bar/ min. Total pumped 5 m3/ bled back 3,5 m3." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Prepared RTTS assy. Performed TBT prior to P/U and M/U 9 5/8' RTTS assy." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 19m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: P/U and M/U 9 5/8' RTTS assy with 5 1/2' pup and drift sub. RIH with same from surface to 19 m. Confirmed and lock circ tool in open position." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 19m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2078m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: RIH with 9 5/8' RTTS assy on 5 1/2' DP from 19 m to 2078 m. ( 748 m/ hr)" "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2078m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Broke circulation with 500 lpm/ 11 bar." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3306m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: RIH with 9 5/8' RTTS assy on 5 1/2' DP from 2078 m to 3306 m. Reduced speed inside 9 5/8' liner - 3 min/ std." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3306m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Took up and down weight at RTTS setting depth, up 164 ton/ down 136 ton. Circulated and cleaned setting area with 800 lpm/ 20 bar. Run in 3 meters to 3309 m and pulled back to setting depth 3306 m/ RTTS packer depth 3298 m. Rotated clockwise and slacked off weight, released torque and had 15 ton down weight to set RTTS packer. Closed MPR at BOP and confirmed line up." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3306m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Pressure tested entire well to 300 bar/ 10 min. Pumped volume 3690 l/ Bled back 3680 l." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3287m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Opened BOP. Picked up with 25 ton OP and released packer. Retracted packerelements. Pulled out to 3287 m and racked back stand in derrick." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3287m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed 3' drift in string. Chased drift down string with 2500 lpm/ 98 bar." "On 2009-05-17, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3287m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Flow checked well on trip tank." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3287m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pumped 5 m3 1,6 sg slug. Chased and allowed to settle." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2506m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: POOH with 9 5/8' RTTS on 5 1/2' DP from 3287 m to 2506 m. Reduced speed while POOH with packer in 9 5/8' liner." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 19m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: POOH with 9 5/8' RTTS on 5 1/2' DP from 2506 m to 19 m. (829 m/ hr)" "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 19m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed PS-21 slips and installed master bushed. Racked back last stand in derrick." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH and LD RTTS assy from 19 m to surface." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor and prepared P/U 8 1/2' BHA." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: PU and RIH with 8 1/2' BHA from surface to 42 m. Checked communication resistance in telescope and evaluated readings. BHA consist of: PD Exceed, Ecoscope, Telescope, Sonicvisjon and Stethoscope." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: TBT prior to radio active source activity. Loaded radioactive source in ecoscope tool." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' BHA from 42 m to 138 m of which, 8x 5' HWDP, Jar and Accelerator. Installed totco ring on top of last 5' HWDP at 138 m. Weight below jar; 7,5 ton - Total BHA weight: 10,5 ton." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS-21 slips." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 464m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH with 5' DP from 138 m to 464 m of which, 3 stand from derrick and 15 singles P/U from cantilever." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 627m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 464 m to 627 m. (652 m/ hr)" "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 627m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Filled pipe and tested MWD at 627 m. Test parameters: 1500 lpm/ 53 bar - 2000 lpm/ 85 bar, 30 RPM/ 1-3 kNm." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 627m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Serviced TDS." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1808m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 627 m to 1808 m. Filled pipe every 600 m. (787 m/ hr)" "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1808m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: TBT with focus on slip and cut. Slipped and cut drilling line. Calibrated block." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2174m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 1808 m to 2174 m. (732 m/ hr)" "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2174m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Changed handling equipment from 5' DP to 5 1/2' DP." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3305m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 2174 m to 3305 m. Filled pipe every 600 m. (646 m/ hr)" "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3394m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Washed down in hole from 3305 m to 3394 m. Parameters: 1800 lpm/ 125 bar, 30 RPM/ 10-14 kNm. Took weight and tag top plug/ cement with 7 ton WOB at 3394 m." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3395m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Drilled top plug/ cement from 3394 m to 3395 m. Parameters: 2000 lpm/ 150-170 bar. 30 RPM/ 11-16 kNm. WOB: 4-7 ton. ROP: 1-2 m/hr. Pulled back to 3385 m for chokedrill." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3385m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed choke drill with involved personnel at 3385 m." "On 2009-05-18, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3401m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH to 3395 m. Drilled top plug/ soft cement from 3394 m to 3401 m. Parameters on top plug: 1800 - 2000 lpm/ 120 -180 bar. RPM 50/ 11-16 kNm. WOB: 2-7 ton. ROP: 0,5 - 1m/ hr. Parameters on cement: 2000 lpm/ 150-160 bar. 40 RPM/ 11-14 kNm. WOB: 2-3 ton. ROP: 20 -25 m/hr." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3413m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Drilled soft cement from 3401 m to 3413 m. Parameters: 2000 lpm/ 150-160 bar. 40 RPM/ 11-14 kNm. WOB: 2-3 ton. ROP: 20-25 m/hr." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3414m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Drilled bottom plug and landing collar from 3413 m to 3414 m. Parameters: 1800 - 2000 lpm/ 120 -170 bar. RPM: 30 - 50/ 11-16 kNm. WOB: 7-10 ton. ROP: 0,5 - 1m/ hr." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3434m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Drilled soft cement in shoe track from 3414 m to 3434 m. Parameters: 2000 lpm/ 148-150 bar. 50 RPM/ 11-14 kNm. WOB: 2-4 ton. ROP: 25 -30 m/hr." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Drilled cement in shoe track from 3434 m to 3440 m. Parameters: 2000 lpm/ 147-150 bar. 50 RPM/ 12-14 kNm. WOB: 2-4 ton. ROP: 25 -30 m/hr." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3441m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Drilled 9 5/8' reamer shoe from 3440 m to 3441 m. Parameters: 2000 - 2200 lpm/ 147-185 bar. 50 RPM/ 12-17 kNm. WOB: 0-2 ton. ROP: 0,5-2 m/hr. String stalled out several times and pressure increased with 20-30 bar." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Timedrilled rest of shoe with steady parameters from 3441 m to 3442 m. Parameters: 2200 lpm/ 180 bar, 60 RPM/ 12-18 kNm. WOB: 0-2 ton. Had no clear indication of going out of shoe. Checked shoe/ rathole twice, OK." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3446m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 4 m new formation and 8 1/2' hole from 3442 m to 3446 m. Parameters: 2200 lpm/ 172 - 176 bar, 60 RPM/ 12-17 kNm, WOB: 1-2 ton. ROP: 1-3 m/hr." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3446m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Checked rathole / shoe with and without rotation, OK." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3446m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pumped 4 m3 LCM pill and displaced same as balanced pill. Parameters: 1000 lpm in DP and 800 lpm through BHA." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3332m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH slowly from 3446 m to 3332 m. Meanwhile pressure tested surface lines prior to FIT." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3332m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pumped 1 m3 OBM to clear MWD tools of any LCM." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3332m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: R/U for FIT, checked line up and flushed lines." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3332m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Performed FIT to 1,55 sg EMW by pressuring up to 68 bar at cement unit. Volume pumped: 919 l/ Bled back: 900 l. Meanwhile changed out drill line guide." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3332m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: R/D FIT equipment." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3332m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Planned maintenance - continued changed out drill line guide." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3332m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Performed static pressure survey to 1,57 sg to check FIT." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3446m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' BHA from 3332 m to 3446 m." "On 2009-05-19, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3461m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled 8 1/2' hole from 3446 m to 3461 m. Parameters: 2366 lpm/ 195 bar, 80 RPM/ 14-17 kNm, WOB: 6-7 ton. ROP: 2-4 m/hr. ECD: 1,37 sg Note: Used max 80-90 RPM until top stabilizer out of shoe. Verified 9 5/8' shoe depth with logging tool to 3441 mMD." "On 2009-05-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 8 1/2' hole from 3461 m to 3465 m. Parameters: 2366 lpm/ 192 bar, 80 RPM/ 13-16 kNm, WOB: 5-7 ton. ROP: 2-4 m/hr. ECD: 1,37 sg" "On 2009-05-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed SCR readings at 3465 mMD/ 2655 mTVD with MW 1,30 sg. MP#1: 30 SPM/24 Bar - 40 SPM/ 34 Bar - 50 SPM/ 46 bar. MP#3: 30 SPM/23 Bar - 40 SPM/ 34 Bar - 50 SPM/ 46 Bar." "On 2009-05-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3471m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 8 1/2' hole from 3465 m to 3471 m. Parameters: 2366 lpm/ 192 bar, 80-90 RPM/ 13-16 kNm, WOB: 4-6 ton. ROP: 2-4 m/hr. ECD: 1,37 sg" "On 2009-05-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3506m. The activity was categorized as 'drilling -- drill' and lasted for 13.2 hours. Operational details: Drilled 8 1/2' hole from 3471 m to 3506 m. Parameters: 2366 lpm/ 186-190 bar, 90-180 RPM/ 13-19 kNm, WOB: 2-6 ton. ROP: 2-6 m/hr. ECD: 1,371 sg. Took survey after connection. Varied drilling parameters to optimise ROP." "On 2009-05-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3506m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed SCR readings at 3506 mMD/ 2659 mTVD with MW 1,30 sg. MP#1: 30 SPM/24 Bar - 40 SPM/ 33 Bar - 50 SPM/ 46 bar. MP#2: 30 SPM/23 Bar - 40 SPM/ 33 Bar - 50 SPM/ 46 Bar." "On 2009-05-20, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3522m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 8 1/2' hole from 3506 m to 3522 m. Parameters: 2366 lpm/ 186-190 bar, 140 RPM/ 14-17 kNm, WOB: 5-6 ton. ROP: 4-6 m/hr. ECD: 1,371 sg. Varied drilling parameters to optimise ROP. At 3510 m lost the PNG funtionality from Ecoscope tool." "On 2009-05-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3542m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole from 3522 m to 3542 m. Parameters: 2385 lpm/ 188-190 bar, 140-150 RPM/ 14-18 kNm, WOB: 5-6 ton. ROP: 3-7 m/hr. ECD: 1,372 sg. Varied drilling parameters to optimise ROP." "On 2009-05-21, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3588m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 8 1/2' hole section from 3542 m to 3588 m MD. Drilling parameters : Flow 2400 lpm / SPP ~185 bar / 140-160 RPM / WOB 2-7 MT / Torque 10-20 kNm / ECD 1,37 / ROP 2-8 m/hrs. Penetration limited by torque and stick/slip. Perfomed MWD survey on connections." "On 2009-05-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3600m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole section from 3588 m to 3600 m MD. Drilling parameters : Flow 2400 lpm / SPP ~185 bar / 160-200 RPM / WOB 5-8 MT / Torque 10-20 kNm / ECD 1,37 / ROP 1-3 m/hrs. Penetration limited by torque and stick/slip." "On 2009-05-22, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3653m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 8 1/2' hole section from 3600 m to 3653 m MD. Drilling parameters : Flow 2400 lpm / SPP ~185 bar / 160-200 RPM / WOB 4-7 MT / Torque 15-20 kNm / ECD 1,36-1,37 / ROP 2-10 m/hrs. Penetration limited by torque and stick/slip. Performed MWD survey on connection." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3675m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole section from 3653 m to 3675 m MD. Drilling parameters : Flow 2400 lpm / SPP ~187 bar / 200 RPM / WOB 6-7 MT / Torque 15-20 kNm / ECD 1,36-1,37 / ROP 2-10 m/hrs. Penetration limited by torque and stick/slip. Performed MWD survey on connection." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled 8 1/2' hole section from 3675 m to 3695 m MD. Drilling parameters : Flow 2400 lpm / SPP ~187 bar / 200 RPM / WOB 4-9 MT / Torque 15-20 kNm / ECD 1,36-1,37 / ROP 2-8 m/hrs. Penetration limited by torque and stick/slip." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Observed 0,5 m2 gradual gain in active. Checked pits and shaker and compared to Geoservice sensors. Picked off bottom and flow checked - well static." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Made decision to POOH for changing BHA. Circulated BHA clear of cuttings at 2400 lpm. Downlinked Powerdrive before POOH according to DDs instructions." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' drilling BHA from 3695 m to 3422 m MD on 5 1/2' DP. Pulled wet pipe." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pumped 5 m3 slug of 1,65 sg OBM. Chased slug to drillfloor and allowed mud level to settle." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Repaired hydraulic leak on aft IR." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2174m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 3422 m to 2174 m MD. Tripping speed 1000 m/hr." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2174m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed from 5 1/2' to 5' handling equipment." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: POOH with 8 1/2' drilling BHA on 5' DP from 2174 m to 178 m MD. Tripping speed 1000 m/hr." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 178m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Flowchecked well on triptanks prior to pulling BHA - well static. Removed auto slips and installed masterbushing and bowls in RT." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Held toolbox talk for laying out BHA. Racked back stand of 5' HWDP. Made up stand of 5' HWDP to accelerator and racked back in derrick. Broke 5' HWDP/jar stand and laid out single for inspection. Picked up new 5' HWDP and made up to stand, racked back stand in derrick." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held toobox talk for handling RA-soruce. Cleared drillfloor of non-essential personnel. Broke connection above Echoscope and removed RA source." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Broke and laid out Stethoscope, Sonicvison, Telescope and Echoscope. Inspected and gauged stabilizers and bit. Laid out 8 1/2' Powerdrive exceed." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleared and tidied drillfloor." "On 2009-05-23, at Well NO 15/9-F-10, a drilling event occurred at a depth of 8m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Held toolbox talk for using manual tongs. Picked up back-up 8 1/2' Powerdrive exceed. Installed bit and bit breaker in RT. Made up 8 1/2' bit to Powerdrive exceed using manual tongs. Picked up and made up Telescope/MWD." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Picked up and made up 2 x 6 7/8' NMDC and AST tool. Picked up and made up 2 x 5 1/2' HWDP singles. Made up stand of jar/5' HWDP and stand of accelerator/5' HWDP. Installed totco ring." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed auto slips." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 581m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 135 m to 581 m MD." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 581m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Made up TDS. Filled DP with 1,30 sg OBM at 2700 lpm. Tested MWD and Powedrive exceed - ok." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1190m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 581 m to 1190 m MD." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1190m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Made up TDS and filled DP with 1,30 sg OBM." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1190m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Serviced and greased TDS." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1722m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 1190 m to 1722 m MD." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1763m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 1722 m to 1763 m MD." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1763m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed from 5' to 5 1/2' handling equipment. Made up TDS and filled DP." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2369m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' drilling BHA on 5 1/2' DP from 1763 to 2369 m MD. Tripping speed 1000 m/hrs. Drawwork stopped by sudden incident." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2369m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Investigated hard trip of drawworks." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2369m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2974m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 2369 m to 2974 m MD. Ran carefully across liner top at 2506 m MD. Tripping speed 600 m/hrs" "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2974m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3618m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 2974 m to 3618 m MD. Tripping speed 650 m/hrs." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Washed down from 3618 m to 3695 m MD. Parameters : 2400 lpm / SPP 190 bar / 60 RPM / Torque 14 kNm." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Took SCR's before start drilling. Jetted bottom of hole." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3705m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 8 1/2' hole section from 3695 m to 3705 m MD. Drilling parameters : Flow 2400 lpm / SPP 180-188 bar / 200 RPM / WOB 2-4 MT / Torque 15-20 kNm / ROP 2-3 m/hr. Penetration limited by stick/slip. Perfomed MWD survey on connection." "On 2009-05-24, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3816m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Issued concent to drill ahead under severe stick/slip conditions. Drilled 8 1/2' hole section from 3705 m to 3816 m MD. Drilling parameters : Flow 2200 lpm / SPP 150-160 bar / 200 RPM / WOB 7-9 MT / Torque 20-30 kNm / ROP 17-20 m/hr. Perfomed MWD survey on connections." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3839m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8 1/2' hole section from 3816 m to 3839 m MD. Drilling parameters : Flow 2200 lpm / SPP ~150 bar / 200 RPM / WOB 7-9 MT / Torque 20-25 kNm / ROP 17 m/hr. Perfomed MWD survey on connections." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3839m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Due to 0,6 m3 gain in active, picked off bottom. Lined up trip tanks and flowchecked - well static." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3863m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 8 1/2' hole section from 3839 m to 3863 m MD. Drilling parameters : Flow 2200 lpm / SPP 155 bar / 200 RPM / WOB 7-9 MT / Torque 20-25 kNm / ROP 17 m/hr. Picked off bottom and recessed operation for repair of TDS blower hose (air cooling system)." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3863m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Made temporary repair on buckled air blower hose on TDS. Meanwhile circulated at 1500 lpm / SPP 81 bar while rotating at 20 RPM." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3863m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Made temporary repair on buckled air blower hose on TDS." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4159m. The activity was categorized as 'drilling -- drill' and lasted for 16.2 hours. Operational details: Drilled 8 1/2' hole section from 3863 m to 4159 m MD. Drilling parameters : Flow 2200-2500 lpm / SPP 190-208 bar / 200 RPM / WOB 9-13 MT / Torque 20-25 kNm / ROP 18-28 m/hrs. Performed MWD survey on connections. Downlinked Powerdrive according to DD instructions." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4167m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 8 1/2' hole section from 4159 m to 4167 m MD. Observed continuos left hand tendency of Powerdrive despite 20% right setting. Reduced ROP to 10 m/hrs and attempted to set Powerdrive to 60% right - still observed left hand tendency. Picked off bottom and reamed stand while confering with Schulmberger support centre." "On 2009-05-25, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4168m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: As recommended by support centre, sent 3 consecutive downlinks to Powerdrive : 1.Reset / 2.Hold / 3.60% right." "On 2009-05-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4170m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 2-3 m 8 1/2' hole to 4170 m MD. Observed no right hand response on Powerdrive with 60% right setting." "On 2009-05-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4205m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Downlinked Powerdrive to 80% right hand setting. Drilled 8 1/2' hole section from 4170 m to 4205 m MD. Drilling parameters : Flow 2500 lpm / SPP ~205 bar / 200 RPM / WOB 7-9 MT / Torque 20-22 kNm / ROP 20 m/hrs. Obtained right hand movement and change in azimuth from 113 to 117 deg." "On 2009-05-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4266m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 8 1/2' hole section from 4205 m to 4266 m MD. Drilling parameters : Flow 2500 lpm / SPP ~207-210 bar / 200 RPM / WOB 9-11 MT / Torque 20-25 kNm / ROP 20-25 m/hrs. Performed MWD survey on connections. Downlinked powerdrive according to DDs instructions." "On 2009-05-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4306m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 8 1/2' hole section from 4266 m to 4306 m MD. Drilling parameters : Flow 2500 lpm / SPP ~213 bar / 200 RPM / WOB 10-12 MT / Torque 20-26 kNm / ROP 25-28 m/hrs. Performed MWD survey on connection. Downlinked powerdrive according to DDs instructions." "On 2009-05-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4306m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Inspected, serviced and greased TDS." "On 2009-05-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4482m. The activity was categorized as 'drilling -- other' and lasted for 10.0 hours. Operational details: Drilled 8 1/2' hole section from 4306 m to 4482 m MD. Drilling parameters : Flow 2800 lpm / SPP ~240 bar / 200 RPM / WOB 9-12 MT / Torque 21-23 kNm / ROP 20-25 m/hrs. Performed MWD survey on connection. Downlinked powerdrive according to DDs instructions. Attmepted to reduce torque by adding Baralube to the mud, obtained no recordable difference." "On 2009-05-26, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4523m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Got problems with DCI system not processing cuttings properly. Picked off bottom and shut down pumps. Discussed situation and decided to continue drilling routing cuttings to skips. Routed cuttings to skips on deck. Continued drilling 8 1/2' hole section from 4482 m to 4523 m MD with reduced penetration rate. Drilling parameters : Flow 2800 lpm / SPP 255-260 bar / 200 RPM / WOB ~7 MT / Torque 18-22 kNm / ROP 10 m/hrs. Performed MWD survey on connection. Meanwhile changed impellers on DCI pumps." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4549m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 8 1/2' hole section from 4523 m to 4549 m MD with reduced penetration rate. Drilling parameters : Flow 2800 lpm / SPP ~260 bar / 200 RPM / WOB ~7 MT / Torque ~20 kNm / ROP 10-15 m/hrs. Tested DCI system after impeller change out. Observed escalating leakage on end hub of DCI manifold. Skips about to be filled - unable to drill ahead." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4549m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Traced spare flange adapter to be in Dusavik base due out on Wednesday boat. Called town and arranged for heli transport of required parts. Circulated hole clean while reciprocating stand. Parameters : Flow 2500-2800 lpm / SPP 213-263 bar / 160-200 RPM / Torque 14-16 kNm." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4182m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Waited on spare parts for DCI to arrive on helicopter. Meanwhile POOH to 4102 m MD to check hole condition." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4102m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Serviced TDS." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4549m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Replaced DCI flange adapter and tested system. Meanwhile reamed back in with 8 1/2' drilling BHA on 5 1/2' DP from 4102 to 4549 m MD. Parameters : Flow 2000-2800 lpm / SPP145-270 bar / 60 RPM / Torque ~15 kNm." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4633m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole section from 4549 m to 4633 m MD. Drilling parameters : Flow 2800 lpm / SPP 262-266 bar / 200 RPM / WOB 7-11 MT / Torque ~21 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions. Got liner spray alarm on mudpump#2." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4633m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Checked out liner spary alarm on mudpump#2. Meanwhile reciprocated stand pumping at 1800 lpm." "On 2009-05-27, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4670m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 8 1/2' hole section from 4633 m to 4670 m MD. Drilling parameters : Flow 2800 lpm / SPP 262-266 bar / 200 RPM / WOB 7-11 MT / Torque ~23 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4720m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled 8 1/2' hole section from 4670 m to 4720 m MD. Drilling parameters : Flow 2800 lpm / SPP 256-264 bar / 200 RPM / WOB 10-12 MT / Torque 20-25 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4720m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Checked out liner spary alarm on mudpump#2. Meanwhile reciprocated stand pumping at 1800 lpm." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4750m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 8 1/2' hole section from 4670 m to 4750 m MD. Drilling parameters : Flow 2800 lpm / SPP 256-264 bar / 200 RPM / WOB 10-12 MT / Torque 21-23 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4750m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Inspected and service fwd/aft PRS. Checked oil on TDS gearbox." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4750m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Made connection and MWD survey." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4790m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 8 1/2' hole section from 4750 m to 4790 m MD. Drilling parameters : Flow 2800 lpm / SPP ~266 bar / 200 RPM / WOB ~10 MT / Torque 20-23 kNm / ROP 20-25 m/hr. Performed MWD survey on connections. Downlinked Powerdrive according to DDs instructions. Recessed operation for changing TDS gearbox oil." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4790m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Changed oil in TDS gearbox due to traces of water in oil sample. Meanwhile circulated at 1000 lpm." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4820m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8 1/2' hole section from 4790 m to 4820 m MD. Drilling parameters : Flow 2800 lpm / SPP ~267 bar / 200 RPM / WOB ~10 MT / Torque 20-23 kNm / ROP 25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4820m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Due to no reduction in active when drilling last stand, lined up to triptanks and flowchecked - well static." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4911m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled 8 1/2' hole section from 4820 m to 4911 m MD. Drilling parameters : Flow 2800 lpm / SPP ~272 bar / 200 RPM / WOB ~7 MT / Torque 20-24 kNm / ROP 25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4911m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed MWD survey. Downlinked Powerdrive and set in neutral. Broke and laid out 5 1/2' single." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: Circulated hole clean while reciprocating stand. Parameters : Flow 1500-2800 lpm / SPP 97-270 bar / 60-200 RPM / Torque ~18 kNm. Circulated two times bottoms up. Verified clean shakers." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held toolbox talk for running WL gyro. Lined up well on trip tank." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Hung off stringin slips with 130 MT downweight. Suspended upper WL sheave in elevator. Suspended lower WL sheave in tugger and slings to samson posts. Made up stuffing box to pump in sub. Set WL depth relative to RT. Stabbed gyro toolstring. Made up FOSV/pump-in sub/stuffing box to DP using IR. Made up cement hose to pump in sub." "On 2009-05-28, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: RIH with gyro on 5/16' EWL from surface to 360 m MD. Initialized gyro and CLL according to Scientific procedures. RIH with 5/16' EWL to 1300 m MD." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- wire line' and lasted for 3.2 hours. Operational details: RIH/pumped gyro on 5/16' EWL from 1300 to 4760 m MD (top of totco ring in BHA). Pumprate 600-1500 lpm, SPP 33-109 bar. Observed pressure build up to 115 bar when landing in totco ring." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Lined up well on trip tank. POOH with gyro on 5/16' EWL from 4760 m to 800 m MD. Logged survey data according to Scientific procedure." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: POOH with gyro on 5/16' EWL from 800 m MD to surface. Logged survey data according to Scientific procedure. Performed tie-in pass to seabed. POOH with gyro to surface." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging down WL." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Cleaned drillfloor for OBM spills. Unhooked cement hose. Broke FOSV/side-entry/pack box using IR and lifted same with tugger whilst comming out with WL toolstring. Laid down toolstring. Rigged down sheaves. Cleared and tidied drillfloor." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4898m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Picked up and made up 5 1/2' space out single from deck. Took upweight with high overpull > 20 MT." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4911m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Stepped up pumprate in increments to 2800 lpm / SPP 293 bar. Reciprocated stand at 60/200 RPM. Circulated bottoms up. Removed master bushing and installed automatic slips." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4710m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: POOH with 8 1/2' drilling BHA from 4911 m to 4859 m MD, took >20 MT overpull. Pumped out of hole with 5 stands of 5 1/2' DP to 4710 m MD at 1500 lpm / 30 RPM." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3985m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 4710 m to 3985 m MD. Pulled wet pipe." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3985m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pumped 5,5 m3 1,60 sg slug at 1200 lpm and chased to drillfloor. Allowed mud levels to settle." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3420m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 3985 m to 3420 m MD." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3420m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Lined up tritanks and flowchecked in shoe - well static." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3420m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed filters on TDS gearbox." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3255m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 3420 m to 3255 m MD." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3255m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pumped slug. Allowed mud levels to settle." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1756m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 3255 m to 1756 m MD. Tripping speed 750 m/hrs." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1756m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Changed from 5 1/2' to 5' handling gear. Dropped 3' drift in 5' DP." "On 2009-05-29, at Well NO 15/9-F-10, a drilling event occurred at a depth of 746m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH with 8 1/2' drilling BHA on 5' DP from 1756 m to 746 m MD. Tripping speed 800 m/hrs." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 296m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' drilling BHA on 5' DP from 746 m to 296 m MD." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 296m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Flowchecked well before pulling BHA - well static. Removed auto slips and installed masterbushing and bowl." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 16m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Recovered totco and 3' drift. Broke and racked back stand of 5' HWDP/accelerator. Broke and laid out 2 x 5' HWDP singles. Broke and racked back stand of 5'HWDP/jar. Broke and laid out AST and 2 x NMDC." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with Telescope and 8 1/2' Powerdrive. Inspected bit and found good for reuse. Broke bit using bit breaker wrench and easytorque." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Broke and laid out Telescope and 8 1/2' Powerdrive Xceed." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Brought jet sub to drillfloor and hung off in RT. Brought 18 3/4' BOP test plug to drillfloor and made up same." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH with 18 3/4' BOP test plug to 139 m MD." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held toolbx talk for testing BOP. Washed across wellhead at 3000 lpm / 10 RPM. Landed BOP test plug at 139 m MD." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 7.5 hours. Operational details: Tested 18 3/4' BOP and IBOPs to 30/345 bar 5/10 min." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Broke out test swadge from TDS. POOH with 18 3/4' BOP test plug from 139 m MD. Broke and laid out test plug and jet sub." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Changed filters on TDS gearbox, still faulty indications. Changed level sensor on TDS gearbox . Meanwhile changed sheared coupling on encoder for drawworks motor #4." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for making up BHA." "On 2009-05-30, at Well NO 15/9-F-10, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Picked up 8 1/2' PD Xceed. Made up 8 1/2' bit to PD Xceed using bit tong and easytorque. Picked up and made up Echoscope, Telescope, Sonicvison and Stethoscope. Established scribeline to Stethoscope when running in." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Picked up and prepared Echosope/neutron for service. Installed RA-source in Echoscope." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Picked up and made up 5' HWDP single. Made up stand of jar/HWDP. Picked up and made up 2 x 5' HWDP singles. Made up stand of accelerator/HWDP. Installed totco ring on top of HWDP." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Removed master bushing. Installed auto slips in RT and hooked up hydraulics." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 138 m to 340 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 381m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Picked up, made up and RIH with 3 x 5' DP to replace stand #6 ." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 626m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 381 m to 626 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 626m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Made up x-over to drillstring. Made up TDS and filled string, confirmed returns." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1237m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 626 m to 1237 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1237m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Made up x-over to drillstring. Made up TDS and filled string. Pumped at 2000 lpm / SPP 106 bar and confirmed MWD functional." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP frpm 1237 m to 1400 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1808m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 1400 m to 1808 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1808m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2171m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' drilling BHA on 5' DP from 1808 m to 2171 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2171m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed from 5' to 5 1/2' handling gear." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2411m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' drilling BHA on 5 1/2' DP from 2171m to 2411 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2411m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2977m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' drilling BHA on 5 1/2' DP from 2411 m to 2977 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2977m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' drilling BHA on 5 1/2' DP from 2977 m to 3422 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3985m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: RIH with 8 1/2' drilling BHA on 5 1/2' DP from 3422 m to 3985 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3985m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up TDS and filled pipe." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4393m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: RIH with 8 1/2' drilling BHA on 5 1/2' DP from 3985 m to 4393 m MD." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4877m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: RIH with 8 1/2' drilling BHA on 5 1/2' DP from 4393 m to 4877 m MD. Made up TDS on each stand run and reamed on way in. Parameters : Flow 1000 lpm / SPP 58-62 bar / 20 RPM / Torque ~15 kNm." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4911m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Established drilling parameters when comming down on stand from 4877 m to 4911 m MD. Downlinked PD Xceed for drilling. Parameters : Flow 2500 lpm / SPP 250 bar / 200 RPM / Torque 15-20 kNm / ECD 1,45-1,46 sg." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4935m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled 8 1/2' hole section fro 4911 m to 4935 m MD. Drilling parameters : Flow 2050-2500 lpm / SPP 179-247 bar / 200 RPM / Torque 18-22 kNm / ROP 12 m/hrs / ECD 1,44-1,45 sg. Investigated ECD dependency on rate : 1,450 @ 2433 lpm / 1,442 @ 2278 lpm / 1,432 @ 2058 lpm. Performed MWD surevey on connection. Obtained ESD value of 1,354." "On 2009-05-31, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4958m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drillied 8 1/2' hole section from 4935 m to 4958 m MD. Drilling parameters : Flow 2400 lpm / SPP ~250 bar / 200 RPM / Torque 21-23 kNm / ROP 25 m/hrs / ECD 1,45-1,46 sg. Observed severe oil leakage from one of the TDS link tilt cylinders." "On 2009-06-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4958m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Halted drilling operation for repair of TDS link tilt cylinder. Dismounted link tilt cylinder and brought to workshop for repair. Re-mounted link tilit cylinder. Meanwhile circulated in hole at 1300 lpm / SPP 85-89 bar. ECD 1,37-1,38 sg." "On 2009-06-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4994m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 8 1/2' hole section from 4958 m to 4994 m MD. Drilling parameters : Flow 2400 lpm / SPP 240-245 bar / 200 RPM / Torque ~20 kNm / ROP 25 m/hrs / ECD 1,44-1,45 sg.Downlinked PD Xceed according to DDs instructions, had to pick off bottom in order to get downlink accepted. Observed high dropping tendency of BHA." "On 2009-06-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5255m. The activity was categorized as 'drilling -- drill' and lasted for 15.8 hours. Operational details: Drilled 8 1/2' hole section from 4994 m to 5255 m MD. Drilling parameters : Flow 2500 lpm / SPP 250-260 bar / 200 RPM / Torque 18-23 kNm / ROP 25 m/hrs / ECD 1,44-1,48 sg. Performed MWD survey on connections. Downlinked PD Xceed according to DDs instructions." "On 2009-06-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5255m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Picked off bottom and circulated cuttings above BHA, Performed sticky test on BHA : 5 min static and then picking up. String came free at 225 MT upweight, last p/u weight 196 MT." "On 2009-06-01, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5255m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated bottoms up while reciprocating string in order to reduce drag in well. Parameters : Flow 2000-2500 lpm / SPP 176-260 bar / 150-200 RPM / Torque 17-19 kNm / ECD 1,48=>1,45 sg." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5255m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Stopped rotation. Circulated at 2500 lpm. Took p/u weight 196 MT. Performed two sticky tests : 3 min - 198 MT p/u and 8 min 205 MT p/u weight. Downlinked Stethoscope. Positioned string with bit at 5249 m MD / probe depth 5215 m MD. Obtained pressure sample of 87,17 bar at 5215 m MD." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5280m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 8 1/2' hole section from 5255 m to 5280 m MD as adviced by geologist. Drilling parameters : Flow 2500 lpm / SPP 250-260 bar / 200 RPM / Torque 18-23 kNm / ROP 25 m/hrs / ECD 1,47-1,49 sg. Performed MWD survey on connection." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5280m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Downlinked Stethoscope. Positioned string with bit at 5264 m MD / probe depth 5230 m MD. P/u weight 205 MT. Obtained pressure sample of 88,07 bar at 5230 m MD." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5300m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 8 1/2' hole section from 5280 m to 5300 m MD as adviced by geologist. Drilling parameters : Flow 2300 lpm / SPP ~231 bar / 200 RPM / Torque ~22 kNm / ROP 25 m/hrs / ECD 1,48-1,49 sg. Performed MWD survey on connection." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5300m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Downlinked Stethoscope. Positioned string with bit at 5287 m MD / probe depth 5253 m MD. P/u weight 197 MT. Obtained pressure sample of 89,51 bar at 5253 m MD. High p/u weight when comming free with string (~230 MT), came down with string, started rotation and came free, no pack off tendency." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5314m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 8 1/2' hole section from 5300 m to 5314 m MD as adviced by geologist. Drilling parameters : Flow 2300 lpm / SPP ~233 bar / 200 RPM / Torque ~21 kNm / ROP 15-25 m/hrs / ECD 1,48-1,49 sg." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5331m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 8 1/2' hole section from 5314 m to TD at 5331 m MD as adviced by geologist. Drilling parameters : Flow 2300 lpm / SPP ~235 bar / 200 RPM / Torque ~20 kNm / ROP 15 m/hrs / ECD 1,49 sg." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5331m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated hole clean while reciprocating string between 5331 m and 5320 m MD. Parametes : Flow 2300 lpm / SPP ~235 bar / 150-200 RPM / Torque 17-19 kNm / ECD 1,47-1,48 sg. Downlinked PD Xceed for tripping out." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5320m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.8 hours. Operational details: Set back one stand and continued to circulate well clean reciprocating stand beetween 5320 m and 5380 m MD. Parameters : Flow 2300 lpm / SPP 232-236 bar / 150-200 RPM / Torque ~18 kNm / ECD 1,48 sg." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5215m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 5320 m to 5215 m MD. Parameters : Flow 2200 lpm / SPP 230-240 bar. Took >20 MT overpull at 5215 m MD. Attempted to rotate to move pipe down - negative. Worked string free by comming down with 60 MT downweight and applying 33 kNm - pipe free. Standpipe pressure stable around 235 bar. Washed and reamed upwards 2200 lpm / 20 RPM, took 20-25 MT overpull and string stalled out. Worked string free by setting down full string weight. Washed and reamed through tight area with 2200 lpm / 60-120 RPM." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4960m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Backreamed with 8 1/2' drilling BHA on 5 1/2' DP from 5320 m to 4960 m MD. Parameters : Flow 2300 lpm / SPP 239-226 bar / 60 RPM / Torque ~14 kNm / ECD 1,45-1,46 sg." "On 2009-06-02, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4084m. The activity was categorized as 'formation evaluation -- log' and lasted for 7.5 hours. Operational details: Backreamed from 4960 m to 4084 m MD while logging interval. Parameters : Flow 2300 lpm / 226=>207 bar / Rotation 60 RPM / Torque 16=>12 kNm / ECD 1,46=>1.43 sg / Pulling speed 4,5 m/min." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3665m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.0 hours. Operational details: Backreamed from 4084 m to 3650 m MD while logging interval. Parameters : Flow 2300 lpm / 207=>192 bar / Rotation 60 RPM / Torque 12=>11 kNm / ECD 1,43=>1.41 sg / Pulling speed 4,5 m/min." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 3665 m to 3422 m MD inside 9 5/8' liner shoe. Pulled wet pipe." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Flowchecked - well static. Pumped 5 m3 1,65 sg slug and allowed mud level to settle." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3223m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 3422 m to 3223 m MD." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2175m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: POOH with 8 1/2' drilling BHA on 5' DP from 3223 m to 2175 m MD. Tripping speed 465 m/hr." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2175m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed from 5 1/2' to 5' handling equipment. Pumped 5 m3 1,65 sg slug and allowed mud level to settle." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 2175 m to 1360 m MD. Tripping speed 362 m/hr. Problems with aft PRS claw." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1360m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Troubleshot aft PRS claw." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 1360 m to 139 m MD. Tripping speed 542 m/hr." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Flow checked well prior to pulling BHA - well static. Meanwhile held toolbox talk for handling BHA." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 114m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 8 1/2' drilling BHA. Racked back stand of 5 1/2' HWDP. Removed automatic slip. Installed master bushing." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Broke and laid down jar and accelerator. Racked back stand of 5 1/2' HWDP. Broke and laid down Stethoscope, Sonicvision, Telescope, Echoscope and 8 1/2' PD exceed. Recessed operation due to exhaust fumes on drillfloor (F-99)." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.8 hours. Operational details: Resumed operation on F-10 at 19:30. Serviced and greased TDS. De-isolated equipment. Dressed IR with 3 1/2' dies. Installed 3 1/2' inserts in BX elevator." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for running 3 1/2' DP." "On 2009-06-03, at Well NO 15/9-F-10, a drilling event occurred at a depth of 326m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: RIH with 3 1/2' DP open ended from surface to 326 m MD. Picked up singles from deck. Drifted DP to 2 1/4'. Observed leakage on PS-21 slips." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 326m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed PS-21 from RT. Installed master bushing and bowl." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 353m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIH with 3 x 3 1/2' singles to 353 m MD using manual slips. Changed inserts in BX from 3 1/2' to 5'. Installed and made up 3 1/2' x 5' x-over. Picked up stand of 5 1/2' DP and made up to x-over." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 353m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Removed master bushing and outer ring. Installed PS-30 slips in RT and hooked up same." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 353m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Dressed PS-30 with 5' slips inserts." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1010m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: RIH with 5' DP from 353 m to 1010 m MD. Got incorrect volume in triptanks, well apparently gaining. Investigated situation, suspected partial plugging of DP. Flowchecked for 15 min - lost 200 liter (pipe filling)." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1010m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Looked down DP when in slips and observed that pipe was not filled properly. Made up TDS and filled pipe with approx 200 liter before pressure build up. Performed pump test - 11 bar SPP @ 500 lpm and 33 bar SPP @ 1000 lpm - good match with hydraulic simulations." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1291m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH with 5' DP from 1010 m to 1291 m MD." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2103m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: RIH with cement string from 1291m to 2103m MD." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2103m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Emptied trip tank, moved bent 5' DP in derrick. Changed from 5' to 5 ½' DP handling equipment. Broke circulation with 3000 l/min, 300 bar. (2500 l/min, 229 bar.)" "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3440m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: RIH with cement string from 2103m to 3440m MD." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3440m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Broke circulation at 3440m MD, 500 l/min, 30 bar." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5168m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.5 hours. Operational details: RIH with cement string from 3440m to 5168m MD." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5331m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: Washed down from 5168m to tagging depth, 5331m MD. 500 l/min, 35 bar." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5326m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pulled 5m, staged up pumps, circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm. Simultaneously cleaned pit for mixing new spacer for cement job, due to contamination in first spacer." "On 2009-06-04, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5326m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: Cleaned pit for mixing new spacer for cement job, due to contamination in first spacer." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5326m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued to clean pit and mixing lines. circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5326m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Filled pit with drill water and performed clorine check prior to start mixing cement spacer. Circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5326m. The activity was categorized as 'plug abandon -- other' and lasted for 3.8 hours. Operational details: Mixed cement spacer according to specifications. Simultaneously removed claw from aft PRS. Held tool box talk prior to cement job. Circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5326m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Stopped pumps and rotation, took up weight, needed 230 ton to move pipe, than 200 ton up weight. Needed to rotate to come down, 156 ton. No circulation. Performed line test from cement unit to rigfloor 200 bar, 10 min." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5326m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Mixed cement spacer according to specifications. Circulated with 1000 l/min, 65 bar. 25 rpm, 13-17 kNm." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5329m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Circulated and conditioned mud at 5329m MD. 1000 l/min, 65 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5329m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Toolbox talk prior to pump cement plug." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5329m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Prepared for pumping spacer. Informed engineer and production. cement room had priority for use of air." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5329m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 7m3, 320 strokes 1,47 sg spacer, chased with 0,5m3, 23 strokes OBM. 1000 l/min, 68 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5329m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Mixed and pumped 12,7m3 1,90 sg Silica cement. Displaced to rigfloor with 892 ltr. drill water." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5329m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Displaced cement down string, 48m3, 2200 strokes. 1900 l/min, 110 bar. Reduced rate at 43m3. 1000 l/min, 75 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5010m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: Got back pressure in string while pulling out of cement, connected DDM and pumped 6 strokes, 130 l per stand." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 5010m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Inserted 2 sponge balls, due to back pressure we had to brake first single below DDM." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4900m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Pulled from 5010m to 4900m MD, pumped sponge balls through string. 2500 l/min, 290 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 4900m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Flushed stand pipe manifoild after cement job." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3795m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.8 hours. Operational details: POOH wet with cement string from 4900m to 3795m MD." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3795m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Broke circulation and filled trip tank." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3795m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Pumped 30m3, 1370 strokes Hi-Vis pill. 1300 l/min, 97 bar. Displaced Hi-Vis pill with 30,5m3, 1396 strokes. 1986 l/min, 194 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3795m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: 64 bar backpressure in string after displacement of Hi-Vis pill. Bled back 300 ltr. 0 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3495m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: POOH wet from 3795m to 3495m MD." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3495m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Established circulation 2750 l/min, 290 bar, 25 rpm, 8-10 kNm. Observed 73 bar with 220 l/min when broke circulation. Meanwhile held toolbox talk prior to cement job. Observed good Hi-Vis return at surface." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3495m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Broke off double DP and dropped CST." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3495m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Displaced CST with 1000 l/min, 53 bar. Reduced rate to 500 l/min, 22 bar after 29,6m3, 1355 strokes. When CST enters 3 1/2' DP, observed pressure increase to 26 bar, after 32,7m3, 1492 stroles pumped." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Picked up 5m to 3490m MD. pumped 9m3, 410 strokes, 1,47 sg spacer, 1800 l/min, 140 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Mixed and pumped 10,3m3 1,92 sg 'G' cement. 800 l/min, 30 bar from cement unit." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Displaced cement with rig pumps, 2000 l/min, 125 bar, 50 rpm, 6-8 kNm. Reduced rate to 1000 l/min, 29 bar." "On 2009-06-05, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2951m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH with cement string from 3490m to 2951m MD." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2800m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Continued POOH with cement string from 2951m to 2800m MD." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2800m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: Flushed manifold and pumped 2 sponge balls. 3000 l/min, 297 bar. 60 rpm, 7 kNm. Meanwhile moved rollers and HTS and prepared for L/D 5' DP on deck." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2800m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Pumped and displaced 4,7m3, slug 1100 l/min, 53 bar. Filled trip tank with rigpumps." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2080m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH from 2800m to 2080m MD." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2080m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Changed handling equipment from 5 1/2' to 5' DP. Serviced PRS." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2080m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Tool Box Talk prior to L/D 5' DP on deck." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2080m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Changed inserts in mud bucket." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2080m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Pumped and displaced slug." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2023m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH and L/D 5' DP on deck from 2080m to 2023m MD." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2023m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Held Tool Box Talk with on comming shift prior to L/D 5' DP on deck." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 355m. The activity was categorized as 'plug abandon -- trip' and lasted for 8.2 hours. Operational details: POOH and L/D 5' DP on deck from 2023m to 355m MD." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 355m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Cleared and cleaned rigfloor. Changed to 3 1/2' handling equipment." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: POOH and L/D 1 joint of 3 1/2' DP. POOH and racked 3 1/2' DP on setback from 355m to surface." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Cleared and cleaned rigfloor." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Serviced TDS, FWD and AFT PRS." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to cut & slip drill line." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: Slipped & cut dril line. Meanwhile held Tool Box Talk and performed line test prior to test of cement plug." "On 2009-06-06, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Attempted to pressure test cement plug. Pressured up to 50 bar, than in steps of 20 bar. Observed leak of 0,5-1 bar/min. between steps. At 190 bar pressure flattened out with constant pump rate. Stopped pumping, pressure dropped rapidly to 170 bar. Bled off pressure. Discussed further operation with town. Meanwhile crew had Tool Box Talk prior to run EZSV plug." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.5 hours. Operational details: Meeting about next operation. Decided to continue as per DOP and run EZSV plug. Meanwhile repaired leak on AFT iron roughneck and serviced TDS." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: Prepared and made up 9 5/8' EZSV plug to 3 1/2' DP." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 347m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: RIH with EZSV plug on 3 1/2' DP from surface to 347m MD." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: Changed from 3 1/2' to 5 1/2' DP handling equipment. Emptied trip tank. RIH with EZSV plug on 5 1/2' DP from 347m to 715m MD." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1118m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIH with 9 5/8' EZSV plug from 715m to 1118m MD." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1118m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Moved 17 stands of 5 1/2' DP, not wiped with sponge ballls." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2467m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: RIH with 9 5/8' EZSV plug from 1118m to 2467m MD." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2467m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Broke circulation at 2467m MD, 110 l/min, 14 bar. Meanwhile moved rest 11 stands of 5 1/2' DP not flushed with sponge balls." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2467m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Flushed and verified line up from cement unit through TDS and BOP kill line for test of cement plug." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2467m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Attempted to test cement plug to 195 bar. Observed 10 bar drop in 10 min. Than drop increased." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2467m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Flushed lines, meanwhile function tested BOP." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2560m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: RIH with 9 5/8' EZSV plug from 2467m to 2560m MD." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2560m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Set EZSV plug as per Halliburton procedures. Released from and pulled RT out of same." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2555m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Installed TIW and pump in sub, lined up to cement unit." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2555m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Verified line up, performed line test from cement unit, 200 bar, 10 min." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2555m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Pressure tested EZSV plug from above to 165 bar 10 min, OK." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2555m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Tool Box Talk prior to cement job." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2555m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.5 hours. Operational details: With cement unit, mixed and pumped 10,3m3 1,92 sg 'G' cenent slurry, displaced to rigfloor with 892 ltr. drill water. With rig pumps, displaced cement with 23,1m3, 1057 strokes of 1,32 sg OBM. 1800 l/min. Reduced pump rate to 1000 l/min. after 18m3, 821 strokes." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 2300m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH from 2555m to 2300m MD, dropped 2 x sponge balls. Circulated 1,5 x string volume 33m3, 1505 strokes." "On 2009-06-07, at Well NO 15/9-F-10, a drilling event occurred at a depth of 347m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.5 hours. Operational details: POOH with EZSV RT from 2300m to 374m MD. Max. tripping speed 1200 m/hr." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 347m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Changed handling equipment from 5 1/2' to 3 1/2' DP." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH with 9 5/8' EZSV plug RT on 3 1/2' DP from 347m to surface." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Tool Box Talk prior make up and run 13 3/8' EZSV plug." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Changed to 5' inserts in elevator. Made up 13 3/8' EZSV plug to 5' stand according to Halliburton procedures. Plug set as bridge plug. (closed end)" "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Installed 5' inserts in PS-30 slips. Cleaned and cleared rigfloor." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 530m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.2 hours. Operational details: RIH with 13 3/8' EZSV plug from surface to 530m MD." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1590m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.5 hours. Operational details: RIH with 13 3/8' EZSV packer from 530m to 1590m MD. Filled string every 5 stands." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1590m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Set 13 3/8' EZSV plug at 1590m MD according to Halliburton procedure." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1590m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Cleared and cleaned rigfloor prior to POOH." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1536m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH with 13 3/8' EZSV plug RT from 1590m to 1536m MD. Pumped slug, filled trip tank." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 325m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH with 13 3/8' EZSV plug RT from 1536m to 325m MD." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 325m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed from 5 1/2' to 5' handling equipment. Tool Box Talk prior to L/D 5' DP on deck." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: L/D on deck 5' DP from 325m to surface." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: B/O EZSV plug RT, inspected, cleaned and L/D on deck." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Changed to 5 1/2' inserts in elevator. P/U and M/U Bull nose to 5 1/2' stand. Changed to 5 1/2' inserts in PS-30 slips." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1590m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: RIH with Bull nose on 5 1/2' DP from surface to 1590m MD, tagged 13 3/8' EZSV plug with 5 ton at 1590m, pulled 5m. Meanwhile held Tool Box Talk prior to displace to 1,51 sg OBM from 1585m MD to surface." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1585m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: Displaced Well, kill / choke line, chokemanifoild from 1,32 sg OBM to 1,51 sg OBM." "On 2009-06-08, at Well NO 15/9-F-10, a drilling event occurred at a depth of 687m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: POOH with Bull nose from 1585m to 687m MD." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH with Bull nose from 687m to surface." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Cleared rigfloor. Removed PS-30 slips. Installed master bushing. Held Tool Box Talk." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: P/U Wear Bushing Running Tool from deck. Installed same with jet sub below." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH with WB RT on 5 1/2' HWDP / DP from surface to 140m." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Jetted Well Head / Wear Bushing. 2600 l/min, 45 bar." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Connected RT to Wear Bushing according to Vetco procedures. Needed 50 ton to pull wear bushing free." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH with Wear bushing from 140m." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: B/O Wear Bushing, racked last stand. Broke Jet sub off wear bushing RT. Scormarks outside wear bushing." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: Made up SRT with jet sub below. RIH to jet Well Head, pull MS-seal, jet again and POOH." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: With closed annular, pulled MS-seal. 15 ton over pull. Pulled 1,5m no pressure on choke." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Opened annular, flow checked open well, well static." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: POOH with MS-seal from 138,5m to surface. Re-engaged RT in j-slot. Attempted to remove MS-seal from RT, no go. L/D RT and MS-seal." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U wear Bushing RT, removed old WB, installed new." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH with wear bushing to 138,5m. Washed down 2775 l/min, 46 bar, 4 rpm. Set wear bushing according to Vetco procedures." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH with wear bushing RT, re-set tool and L/D on deck." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Changed dies in AFT AR prior to collar run. Meanwhile cleaned rigfloor after wear bushing run." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U cutting tool and tested same, knives activated at 20 strokes, 440 ltr / hrs, 10 bar. RIH 2 stands." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 80m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed from Master bushing to PS-21 slips." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1580m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.8 hours. Operational details: RIH with 13 3/8' casing cutters from 80m to 1580m MD." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1580m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Took up/down weight, 116/105 ton. Free rotation weight, 110 ton, 4-6 kNm." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1590m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Tagged 13 3/8' EZSV plug, set down 3 ton, 1589,9m. MD" "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1580m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled 10 m. started pumps, 550 l/min, 62 bar. Stopped pumps." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1580m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Started rotation, 100 rpm, 4-6 kNm, started pumps, 540 l/min, 60 bar. After 3-4 min, observed pressure drop from 60 bar to 18-19 bar. Continued for 2-3 min. Stopped rotation and pumps. Flow checked." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1580m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled 1,5m started pumps, 300 l/min, 18 bar. Slacked off string to 1580, took weight, 2 ton, pressure dropped to 6-8 bar." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1580m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped and displaced 4,7m3 1,71 sg slug." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: POOH with 13 3/8' casing cutter from 1580m MD, to surface." "On 2009-06-09, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Changed saver sub in DDM." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Continue to change saver sub in DDM." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Broke off X/O above cutters." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U wear Bushing RT." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH with WB RT from surface to 140m." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Retreived wear bushing, 1-2 ton over pull." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with wear bushing from 140m to surface." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/D wear bushing and RT on deck." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 77m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: P/U and RIH with spear assembly. 2 stands of 8' DC from set back and 3 singles from deck." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 77m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Serviced TDS, inspected for loose items prior to pulling casing." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH to setting depth at 141,8m" "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Engaged spear in 13 3/8' casing as per Smith procedure. Pulled casing free with 286 ton on weight indicator. 75 ton overpull." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Pulled up 2m, circulated out old mud as per mud eng. instructions. 3000 l/min, 63 bar." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped and displaced 1m3 1,71 sg slug." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1443m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: POOH with 5 1/2' HWDP, 8' DC and 13 3/8' casing from 1580m to 1443m." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1443m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: M/U TDS and pumped remaining 3,6m3 1,71 sg slug." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1443m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to rig up casing handling equipment." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1440m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Set hanger in slips. Released spear as per Smiths instruction." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1440m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Rigged up 13 3/8' casing handling equipment." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1440m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Transport frame for 13 3/8' casing tong could not run to well certer. Guides on weels too big. Trouble shot." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1440m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Disconnected guide wheels, grinded 1cm off guides." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1440m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Installed wheels on weatherford casing tong. Adjusted and function tested tong." "On 2009-06-10, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1435m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Broke 13 3/8' casing hanger, removed with crane. Broke out 1 more joint.," "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Broke out 2 joints of 13 3/8' casing. Trouble with catwalk conveyer." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1399m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Trouble shot catwalk conveyer." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Fine tuned link tilts and Weatherford tong movements." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1118m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.8 hours. Operational details: POOH and L/D 13 3/8' casing on deck." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1064m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH and L/D 13 3/8' casing from 1118m to 1064." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1064m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Held Tool Box Talk with oncoming crew prior to POOH with 13 3/8' casing." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 11.0 hours. Operational details: POOH with 13 3/8' casing from 1064m to surface." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Rigged down casing equipment." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held Tool Box Talk with oncoming crew prior to rig down casing equipment." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Rigged down casing equipment." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to run and set seat protector." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U seat protector RT, installed seat protector." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH with seat protector on 5 1/2' HWDP / DP." "On 2009-06-11, at Well NO 15/9-F-10, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Jetted well head. Set seat protector according to Vetco procedures." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with seal protector RT. Re-set NSP RT, L/D same on deck." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Tool Box Talk prior to RIH with 3 1/2' cement stinger on 5 1/2' DP." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed to 3 1/2' inserts in elevator. Installed PS-21 slips." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 356m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Changed dies in iron roughneck and PS-21 slips." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 356m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: RIH with 3 1/2' DP from surface to 356m" "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 356m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Changed from 3 1/2' to 5 1/2' pipe handling equipment." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1481m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: RIH with cement string from 356m to 1481m MD." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1481m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to spotting Hi-Vis pill." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1481m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Broke circulation and verified steady parameters. 3040 l/min, 290 bar. RIH from 1480m to 1580m MD." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1580m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pumped and displaced 30m3 1,51 sg Hi-Vis pill. 3000 l/min, 267 bar." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH from 1580m to 1485m MD." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Circulated bottoms up at 1485m MD. 3000 l/min, 260 bar." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and installed pump-in sub assembly." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped 15m3 1,70 sg spacer. 1330 l/min, 62 bar. Chased to rig floor with 800 ltrs. OBM." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Troubleshot blockage from cement tank to surge tank." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Mixed and pumped 41,9m3 1,92 sg 'G' cement slurry." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: B/O and L/D pump-in sub assembly." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: POOH with cement string from 1485m to 1100m MD." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Inserted 2 sponge balls and flushed string. 3200 l/min, 275 bar, 60 rpm, 2 kNm. Meanwhile filled trip tank." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pumped and displaced 4,7m3 1,71 sg slug." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Held Tool Box Talk prior to L/D 5 1/2' DP on deck. Meanwhile troubleshot HTS conveyor." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 629m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: POOH and L/D 5 1/2' DP from 1100m to 629m MD." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 629m. The activity was categorized as 'plug abandon -- wait' and lasted for 5.5 hours. Operational details: Waited on cement to set up. meanwhile troubleshot malfunction on HTS conveyor belt." "On 2009-06-12, at Well NO 15/9-F-10, a drilling event occurred at a depth of 528m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH and L/D 5 1/2' DP from 629m to 528m MD." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 356m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Continued POOH and L/D 5 1/2' DP from 528m to 356m MD." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 356m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Held tool Box Talk. Changed from 5 1/2' to 3 1/2' handling equipment. Broke and L/D X/O's." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH with 3 1/2' cement string from 356m to surface. Racked same in derrick." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor, held tool Box Talk prior to change handling equipment and RIH with jetting tool." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed from 3 1/2' to 5 1/2' handling equipment." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: RIH with Bull nose and Jetting tool from surface to 1100m MD." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- wait' and lasted for 0.5 hours. Operational details: Waited on cement to set up. Meanwhile performed rig maintenance." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'drilling -- casing' and lasted for 6.8 hours. Operational details: Waited on cement. Meanwhile serviced AFT PRS, checked breakes and oil level." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Broke circulation, 400 l/min, 12 bar." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lined up and performed line test, 98 bar, 10 min. Verified line up by applying 10 bar on line, and opened HCR and IBOP." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pressure tested cement plug to 98 bar, 30 min. Pumped 1,21m3. Meanwhile held Tool Box Talk prior to displace well to sea water." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Bled off pressure. Got 1,15m3 in returns." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lined up and displaced surface lines to base oil. C & K manifolds, bleed off, poor boy de-gasser and trip tank." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 1100m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Displaced well to treated sea water as per pumping plan. 2500 l/min, 83 bar." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: POOH with riser jetting tool from 110m to 148m" "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Flushed C & K manifoild with treated sea water. 650 l/min, 3 bar." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped 15m3 Hi-Vis pill to displace riser. 3080 l/min, 43 bar." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Displaced Hi-Vis pill with sea water, and pumped til clean returns. 3475 l/min, 64 bar. Pulled 1 stand every 15 min, rotated 5-10 rpm." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH from BOP to surface. Held Tool Box Talk. L/D 16' jetting tool on deck." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Tool Box Talk. P/U and installed Seat protector RT." "On 2009-06-13, at Well NO 15/9-F-10, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH with seat protector RT from surface to 120m." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued to RIH from 120m to 148m. Connected seat protector. Jetted Well head. 2950 l/min, 33 bar." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH with seat protector from 148m to surface." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Disconnected Bull nose, jet sub and seat protector from RT and L/D RT." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Tool Box Talk. Made up side entry sub assembly, closed annular, blew air down choke line to drain BOP." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Tool Box Talk and preparations for nippling down diverter." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Nippled down diverter." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Nippled down bell niple." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Nipled down and skidded BOP to test stump." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Completed nippling down and skidded BOP to test stump." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to connecting Claxton tool." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed master bushing, ran Claxton tool through, installed master bushing, connected stand of DP." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: M/U Claxton tool to BOP joint. Meanwhile prepared tention system for dis-assembly." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed scaffold from BOP joint." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Transferred tension from cylinders to TDS. Informed production to shut in." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Nippled down tension cylinders. Meanwhile ran guide wire and hot stab." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Moved moonpool hatches from BOP joint." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Unlock TBC. Primary release ineffective. Unlocked TBC secondary release." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Retreive hot stab and guide wire." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: P/U 2m and installed debris cap. Continued P/U until Claxton tool at rotary table. Racked 1 stand 5 1/2' DP." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled BOP joint to rotary level." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held Tool Box Talk prior to install spider." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed HPDR spider." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed fairing and broke flange connection. Meanwhile cleaned in shakers and re-assembled pump 1." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Disconnected at bottom of BOP joint, L/D same on deck." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: P/U splash zone joint, set in spider, disconnected and L/D on deck." "On 2009-06-14, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with HPDR, L/D on deck." "On 2009-06-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Continue POOH with HPDR, L/D on deck." "On 2009-06-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Cleaned and cleared rigfloor. Closed hatches on lower deck. Removed scaffolding. Prepared to run corrotion cap." "On 2009-06-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Cleared rigfloor for excess equipment. Attempted to inspect well head, lost communication with camera. Meanwhile performed general rig maintenance. Prepared for skidding." "On 2009-06-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 4.5 hours. Operational details: Changed blower hose, cleaned shakers, pits and broke riser doubles. Meanwhile repaired camera on ROV." "On 2009-06-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: ROV inspected Well Head with camera. Meanwhile continued to change blower hose and general cleaning." "On 2009-06-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Ran and installed corrosion cap and pumped inhibitor. Cut hose and retreived mini reel and tugger to surface." "On 2009-06-15, at Well NO 15/9-F-10, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed hatch covers in moonpool and removed bridge from cantilever to prosess module. ***End of operation for F - 10.***" "On 1997-11-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: PICKED UP 8 1/2' KICK OFF BHA; AKO MACH 1 XL WITH 1,2 DEGR SETTING. TESTED MOTOR, OK. MADE UP MWD GR/RES/DIR AND LOAD TOOL." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONTINUED TO MAKE UP BHA; MADE UP 8 1/2' PDC BIT WITH 8 3/8' NEAR BIT REAMER. CHECKED SCRIBE LINE AND PICK UP NEW DRILLING JAR." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 956m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: RIH TO 956M. RECORDED SERIAL NO'S ON HWDP." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 956m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: FILLED STRING AND CHECKED MWD PULSES, OK. CHANGE ELEVATOR TO PICK UP 5' DP." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1323m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: PICKING UP 5' DP FOR DRILLING. CURRENT DEPTH 1323M" "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2053m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: CONTINUED TO PICK UP 5' DP TO 2053M. TOTAL P/UP 114 JT." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2138m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: PRECAUTIONARY WASH FROM 2053M TO 2138M." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2178m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: WASHED CMT FROM 2138M TO CSG WINDOW AT 2178M. WORK PIPE TO ORIENT TOOL FACE AN HIT WOODEN CROWN BLOCK BUMPER WITH TRAVELLING BLOCKS." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2178m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: INSPECTED CROWN BLOCKS AND TRAVELLING BLOCKS. FOUND WOODEN BUMPER AND CLAMPS BROKEN. REMOVED DAMAGED PARTS TO DRILLFLOOR. PERFORMED VISUAL INSPECTION TO DERRICK STRUCTURE AND NO DAMAGE WAS FOUND." "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2231m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: WASHED DOWN WITH 400 L/MIN TO OUTSIDE WINDOW AND OBSERVED SLIGHT PACK OFF. PULLED INTO WINDOW, NO OVERPULL. CONTINUED WASHING W/400 L/MIN TO 2223M. INCREASED PUMP RATE TO 1800 L/MIN AND CLEAN HOLE UP TO WINDOW. DRESSED INCONSISTENT CMT FROM 2223 TO FIRM CMT AT 2231M" "On 1997-11-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2243m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: TIME DRILLED IN ORIENTED MODE TO KICK OFF WELL FROM 2231M TO 2243M. HELD TOOLFACE AT 90 DEGR LEFT. 60-70% CMT IN CUTTINGS AT 2243M." "On 1997-11-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2277m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONTINUED TIME DRILLING FROM 2243M TO 2268M, ROTATED TO 2277M. GOT 100% FORMATION 2250M." "On 1997-11-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2283m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: CONTINUED DRILL 8 1/2' HOLE IN ORIENTED MODE FROM 2268M TO 2283M." "On 1997-11-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2283m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: PUMP WITH REDUCED RATE AND RECIPROCATE PIPE WHILST CLEARING CUTTINGS CHUTE BETWEEN SHAKERS SCREW CONVEYERS AND BIG BAG FILLING STATION." "On 1997-11-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2345m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: CONTINUED ORIENTED DRILLING FROM 2283M TO 2345M. NOT ABLE TO GET PLANNED BUILD RATE." "On 1997-11-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2345m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE UNTIL SHAKERS CLEANED UP, TOTAL 120% HOLE VOLUME. FLOW CHECKED, WELL STATIC." "On 1997-11-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: PUMPED SLUG AND POOH. RE-SLUG PIPE, CONTINUED POOH." "On 1997-11-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: LAID DOWN NEAR BIT ROTATION STABILIZER, BROKE BIT. DOWNLOADED MWD AND CHANGED SETTING ON AKO TO 1,4 DEGR. MADE UP ROCK BIT. FOUND 1 DP TO BE MISSING FROM STRING, ALL DEPTHS ON TODAYS REPORT ARE ADJUSTED ACCORDINGLY= -9,5M." "On 1997-11-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2345m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: RIH TO 2312M. FILLED PIPE AT 1000M AND AT CSG WINDOW AT 2110M. TRAVEL THROUGH CSG WINDOW, NO OBSTRUCTIONS. PRECAUTIONARY WASH/ROTATE TO BTM AT 2345M." "On 1997-11-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2350m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: DRILLED IN ROTATION FROM 2345M TO 2350M. TAKE SCR AND ORIENTED STRING TO CONTINUE SLIDING." "On 1997-11-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2619m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 2350M TO 2619M. ROTATED START AND END OF EACH STAND AND ORIENTED 18-20M IN MIDDLE OF EACH STAND TO TURN WELL TO LEFT AND TO DROP ANGLE." "On 1997-11-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2619m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: GEOSERVICE COMPUTER SERVER CRASHED, RE-STARTED SYSTEM. CIRCULATED AND RECIPROCATED PIPE." "On 1997-11-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2744m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: CONTINUED DRILLING FROM 2619M TO 2744M. REAMED ALL STANDS 2 TIMES IN CONNECTIONS." "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2808m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING FROM 2744M TO 2808M. ORIENTED 18-20M IN MIDDLE OF EACH STAND. REAMED STANDS 2 TIMES IN CONNECTIONS." "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2811m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: CONTINUED ORIENTING AND DRILL FROM 2808 TO 2811M." "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: FLOW CHECKED, WELL STATIC. PUMPED LUG AND POOH. FLOW CHECKED AT CSG WINDOW. DOWNLOADED MWD TOOL." "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: MADE UP NEW BIT AND ROTATING NEAR BIT STABILIZER. ADJUSTED SETTING ON AKO TO 1,2 DEGR." "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: RIH WITH BHA. PICKED UP 51 JT 5' DP. RIH TO 1000M AND FILLED PIPE. CONTINUED RIH TO 2100 AND BREAK CIRC, CHECK MWD." "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: FUNCTION TESTED BOP FROM BLUE POD." "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2811m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED TO RIH TO 2773M. PRECAUTIONARY WASH AND REAM TO BTM AT 2811M" "On 1997-11-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2817m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: WASH BTM CLEAN FOR DEBRIS AND DRILLED IN ORIENTED MODE FROM 2811 TO 2817. MOTOR STALLED FREQUENTLY DUE TO BIT WEIGHT SENSIVETY." "On 1997-11-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2850m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: ORIENTED AND ROTATED FROM 2817M TO 2850M. FREQUENTLY STALLING MOTOR. ROTATING MODE; 40-50 M/HR WITH 1-2T WOB." "On 1997-11-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3035m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: CONTINUED DRILLING AND ORIENTING FROM 2850M TO 3035M - LOST RETURNS." "On 1997-11-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3035m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: FLOW CHECKED, WELL STATIC. ATTEMPTED TO REGAIN CIRCULATION BY STAGING PUMPS, 100 % RETURNS BELOW 400 L/MIN. MIXED LCM PILL." "On 1997-11-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3039m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: PUMPED 8 M3 NUT PLUG COARSE, MICA COARSE AND LIGNOCEL (WOOD FIBRE) TOTAL CONCENTRATION, 222,8 KG/M3/1,8 SG. CLEARED SUCTION STRAINERS ON MUD PUMPS PRIOR TO DISPLACING PILL. DURING DISPLACING; DRILLED FROM 3035M TO 3039M NO RETURNS. OBSERVED 17-18 BAR PRESS INCREASE WHEN LCM PASSED BHA. PULLED BACK TO 3030M. STAGED PUMPS TO REGAIN CIRC." "On 1997-11-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2927m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: ATTEMPTED TO ESTABLISH CIRC. LOSSES TO FORMATION STARTED ABOVE 400 L/MIN. LOST TOTAL 43 M3 MUD. POOH WET TO 2927M." "On 1997-11-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2927m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: FLOW CHECKED, WELL STATIC." "On 1997-11-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2530m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: POOH TO 2530M. FLOWED BACK 14 M3, THEN HOLE TOOK NORMAL AMOUNT OF MUD" "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2130m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: CONTINUED POOH INTO CSG WINDOW." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2130m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: ATTEMPTED TO CIRCULATE INSIDE CSG. NOT ABLE TO GET RETURNS ABOVE 400 L/MIN LEVEL. FLOW CHECKED, WELL STATIC. 2 % GAS IN RETURNS." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 667m. The activity was categorized as 'interruption -- lost circulation' and lasted for 4.5 hours. Operational details: PUMPED SLUG. LOST TOTAL 8 M3 MUD TO FORMATION WHEN ATTEMPTING REGAIN CIRC AND PUMP SLUG. POOH. FLOW CHECKED AT 1917M, WELL STATIC. WELL FLOWED BACK DURING TRIP TOTAL 10,6 M3. TOOK NORMAL VOLUME FROM 800M." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: CONTINUED POOH. FLOW CHECKED OK BEFORE PULLED BHA ABOVE BOP." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: RACKED BACK BHA, BROKE BIT AND NEAR BIT STAB." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2000m. The activity was categorized as 'interruption -- lost circulation' and lasted for 4.0 hours. Operational details: MADE UP 3 1/2' MULESHOE ON 290 M 3 1/2' DP AND RIH TO 2000M. NO LOSSES OBSERVED." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2000m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: REPARED HYDRAULIC LEAK ON ACCUMULATOR BOTTLE FOR BLOCK RETRACTION SYSTEM." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3037m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: CONTINUED RIH TO 3030M. MADE UP CMT STAND AND CMT LINE. TESTED CMT LINE WITH 200 BAR." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3037m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: TAGGED BTM AT 3037M. DRILLED DEPTH 3039M. PUMPED 3 M3 SPACER WITH CMT UNIT AND MIXED AND PUMPED 4 M3 1,65 SG CMT SLURRY. DISPLACED CMT WITH RIG PUMPS. NO LOSSES DURING TRIP IN, LOST 1 M3 DURING CEMENTING AND DISPLACING AND 0,2 M3 WHEN CMT ENTERED OPEN HOLE." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2742m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: POOH TO 2742M." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2742m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: CLOSED BOP AND PUMPED 0,55 M3 AND OBTAINED 32 BAR ON CMT PLUG, OK EQUALS 1,69 SG ECD. BLED BACK 0,39 M3 TO CMT UNIT." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2742m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: CIRCULATED HOLE THE LONG WAY. ROTATED AND RECIPROCATED STRING. MAX CIRULATION RATE 2200 L/M. GOT WOOD FIBRE FROM LCM PILL OVER SHAKERS AT END OF CIRCULATION AND REDUCED CIRCULATION RATE TO 1200 L/M. NO MUD LOSSES. FLOW CHECKED, WELL STATIC." "On 1997-11-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 620m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: PUMPED SLUG AND LAID DOWN CMT STAND. POOH TO 620M." "On 1997-11-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: CONTINUED POOH. RACKED BACK 3 1/2' CMT STINGER." "On 1997-11-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.5 hours. Operational details: PICKED UP BHA AND CHECKED OUT AKO, FOUND 4-5 MM BURR ON MIDDLE OF AKO HOUSING. CHANGE TO NEW AKO. CHECKED FOR DEBRIS INSIDE MWD AND DOWNLOAD ED SAME. SET AKO TO 1,2 DEGR AND CHECKED SCRIBE LINE. TESTED MOTOR OK. MADE UP BIT AND NEAR BIT STABILIZER." "On 1997-11-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 549m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: RIH WITH DRILLING AND ORIENTING BHA." "On 1997-11-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1905m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: CONTINUED RIH TO 1905M. AT 0850 HRS. DRILLER SET PIPE ELEVATOR ONTO UPPER PIPE RACKING ARM AND DAMAGED ARM." "On 1997-11-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1905m. The activity was categorized as 'interruption -- maintain' and lasted for 15.0 hours. Operational details: RIG REPAIR: REMOVED DAMAGED HEAD AND CYLINDER ON UPPER RACKING ARM. DISMANTLED TELESCOPE CYLINDER ON STANDLIFT ARM AND MOUNTED SAME ON UPPER RACKING ARM. REPAIRED URA HEAD AND FINGER AND FABRICATED NEW PROTECTION BUMPER FOR FINGER AND ARM TILT. CHANGED BROKEN SAFETY SHEAR PINS FOR RACKING ARM. OBSERVED WELL ON TRIP TANK." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1905m. The activity was categorized as 'interruption -- maintain' and lasted for 6.0 hours. Operational details: CONTINUED RIG REPAIR: NDT INSPECTION WAS CARRIED OUT ON VITAL PARTS ON RACKING HEAD. INSTALLED RACKING HEAD AND TESTED FINGER. FINGER HAD INCOMPLETE TRAVEL. CHANGED FINGER ACTUATOR. WELDED BAR WITH RUBBER BUMPER FOR UPPER RACKING ARM. CUT DOWN HINGED WORK PLATFORM FOR URA DUE TO CRACK DAMAGE. OBSERVED WELL ON TRIP TANK." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1905m. The activity was categorized as 'interruption -- maintain' and lasted for 4.5 hours. Operational details: CONTINUED RIG REPAIR ON UPPER RACKING ARM. RE-ADJUSTED URA FINGER TRAVEL. INSTALLED SAFETY WIRES FOR HEAD AND HEAD PROTECTION. CLEARED DERRICK FOR TOOLS AND PERFORMED FINAL INSPECTION. TESTED UPPER RACKING ARM." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1905m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: PERFORMED SAFE JOB ANALYSIS WITH ALL INVOLVED PERSONNEL. TOPIC; HANDLING PIPE WITHOUT STANDLIFT." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2580m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: RIH TO 2580M." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2580m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: REPAIRED OPERATING CYLINDER ON 5' DP ELEVATOR. FILLED STRING." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2700m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: CONTINUED RIH TO 2700M." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2880m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.5 hours. Operational details: WASHED AND ROTATED FROM 2700M TO 2785M. REAMED AND DRILLED FROM 2785 TO 2880M." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2995m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: DRILLED INCONSISTENT CMT FROM 2880M TO 2983M. CONTINUED DRILLING FIRM CMT FROM 2983M TO 2995M." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2995m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: CIRCULATED HOLE CLEAN DUE TO 20T DRAG INCREASE. REGAINED NORMAL STRING WEIGHT." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3039m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.5 hours. Operational details: DRILLED CMT AT CONTROLLED RATE FROM 2995M TO 3039M. STARTED TO LOOSE FROM 3035M. ATTEMPTED TO ESTABLISH PUMP RATE TO MINIMIZE MUD LOSS, AT 2100 L/MIN: LOST 29 M3/HR. 1500 L/MIN: LOST 16 M3/HR." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3054m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: DRILLED FROM 3035M TO 3054M. VARIED PUMP RATES FROM 2250 -1800 L/M LOSSES 42 - 40 M3/HR." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3054m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: CIRCULATED AND ATTEMPTED TO ESTABLISH 100% RETURNS, NO SUCCESS PUMP RATE 1500 L/M; LOSS RATE 12 M3/HR AND DECLINED TO 5 M3/HR. TOTAL LOSS 45,3 M3 MUD TO FORMATION." "On 1997-11-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: POOH WET TO 2940M. GOT TOTAL FLOWBACK OF 18,2 M3 FROM FORMATION. RIH TO 3050M." "On 1997-11-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE WITH 1500 L/M. LOST 22,4 M3 MUD TO FORMATION." "On 1997-11-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1074m. The activity was categorized as 'interruption -- lost circulation' and lasted for 4.5 hours. Operational details: POOH 25 T OVERPULL IN SECTION 2265-2260M. WORK OBSTRUCTION, OK. FLOW CHECKED INSIDE CSG, WELL STATIC. CONTINUED POOH. HOLE STARTED TO TAKE CORRECT AMOUNT FOR PIPE DISPLACEMENT FROM 1400 M. TOTAL FLOW BACK FROM FORMATION DURING TRIP: 23,2 M3." "On 1997-11-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: CONTINUED POOH WITH DRILLING BHA. FLOW CHECKED, OK BEFORE PULLING ABOVE BOP. RACKED BACK BHA." "On 1997-11-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2010m. The activity was categorized as 'interruption -- lost circulation' and lasted for 6.0 hours. Operational details: MADE UP 3 1/2' MULESHOE ON 3 1/2' DP, TOTAL 290 M AS CEMENTING STINGER CONTINUED RIH WITH 5' DP TO 2010M." "On 1997-11-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2010m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WAITED ON WEATHER DUE TO HIGH WIND, 26-30 M/S AND RIG HEAVE 2 M. WIND SPEED PREDICTIONS INDICATED MORE HEAVE THAN OPERATIONAL LIMITS." "On 1997-11-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: MADE UP DRILL PIPE HANG OFF TOOL AND RIH TO WELLHEAD. HUNG OFF CEMENT STRING AT 2121M AT 1820 HRS. POOH WITH LANDING STRING." "On 1997-11-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: CONTINUED WAITING ON WEATHER DUE TO HIGH WIND, 25-32 M/S AND MAXIMUM HEAVE 9,M - 6,M." "On 1997-11-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONTINUED WAITING ON WEATHER DUE TO HIGH WIND 22-29 M/S. RIG HEAVE 4,5 -5,2 M. AT REPORT TIME." "On 1997-11-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: CONTINUED WAITING ON WEATHER DUE TO HIGH WIND, 23-30 M/S, RIG HEAVE; 4,6- 9,7 M." "On 1997-11-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONTINUED WAITING ON WEATHER DUE TO HIGH WIND, 20-30 M/S RIG HEAVE 4,9-7,9 M." "On 1997-11-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: CONTINUED W.O.W. WIND 20-30 M/S, RIG HEAVE 4.5M - 5.5M, MAX 8.5M." "On 1997-11-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONTINUED W.O.W. WIND 20-30 M/S, RIG HEAVE 4M- 5M, MAX 7.6M." "On 1997-11-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: CONTINUED W.O.W. WIND 26-32 M/S, RIG HEAVE 5.0-5.5M, MAX 8.5M. RAPID, REPEATED HIGH HEAVE 7.0-8.5M FROM 0730. DISPLACED RISER TO SEAWATER AND DISCONNECTED AT 0850 HRS. DEBALLASTED RIG TO SURVIVAL DRAFT AT 1000 HRS." "On 1997-11-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 14.0 hours. Operational details: CONTINUED W.O.W. WIND 32 M/S DECREASING TO 20 M/S THEN INCREASING TO 25 M/S. HEAVE 5.5M DECREASING TO 4.0M THEN INCREASING TO 5.0M." "On 1997-11-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2121m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONTINUED W.O.W. WIND 16-22 M/S AND SLOWLY SUBSIDING. HEAVE 3.3-4.3M AND SLOWLY SUBSIDING." "On 1997-11-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: W.O.W. WIND 22 M/S DECREASING TO 16 M/S. SEAS 6-8 M DECREASING TO 3-5 M. HEAVE 3M DECREASING TO 1.8M." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONTINUED W.O.W. WIND PERSISTED AT 16 M/S. SEAS DECAYED TO 4M, HEAVE TO 1.5M WITH OCCASIONAL PEAKS OF 1.8M. MADE UP DIVERTER HANDLING TOOL AND PREPARED TO RECONNECT LMRP." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: JUMPED ROV AND POSITIONED RIG TO RECONNECT LMRP. LATCHED LMRP AND PULL TESTED WITH 25T OVERPULL. PRESSURE TESTED CHOKE/KILL LINES TO 35/345 BAR. OPENED CHOKE/KILL LINES AND CHECKED FOR FLOW/PRESSURE." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: RIH W/ DP RETRIEVAL STRING. DISPLACED RISER TO 1.53 SG MUD AND FLUSHED BOP BETWEEN SHEAR RAMS AMD LOWER PIPE RAMS. OPENED SR AND MADE UP RETRIEVING STRING INTO EDPHOT." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: CLOSED LOWER ANNULAR PREVENTER AND TESTED EX GASKET IN LMRP CONNECTOR TO 30 BAR. OPENED LPR AND CHECKED PRESSURE - 12 BAR. FLUSHED STACK DOWN KILL LINE AND UP UPPER CHOKE THROUGH POOR BOY DEGASSER - MAX GAS 5.8% STABILIZED AT 4-5%." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: FLOWCHECKED WELL ON CHOKE LINE. OPENED LAP AND FLOWCHECKED WELL ON RISER." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2025m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: CIRCULATED AND CONDITIONED MUD. POOH TO 2096M. CIRCULATED BOTTOMS UP AT 2000 LPM MAX. MAX GAS 8.8% BOTTOMS UP FROM WELLHEAD. GAS STABILIZED AT 2%. POOH. BROKE OUT EDPHOT AND REMADE EDPHOT STAND AND RACKED IN DERRICK." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3054m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.5 hours. Operational details: M/U CEMENTING STAND AND RIH TO 3054M. BROKE CIRCULATION SEVERAL TIMES WHILE RIH TO BALANCE MUD. NO FILL - NO MUD LOSSES." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3054m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: BROKE CIRCULATION AT 250 LPM WITH NO LOSSES. INCREASED RATE TO 1000 LPM AND BEGAN LOSING MUD AT 15 M3/HR. REDUCED CIRCULATING RATE TO 500 LPM - LOSSES AT 12 M3/HR. REDUCED CIRCULATING RATE TO 250 LPM - LOSSES AT 9 M3/HR. FLOWCHECKED - HOLE STOOD FULL WITH 30 BAR BACK PRESSURE ON DP. BLED OFF DP PRESSURE AND POOH 1 STAND TO 3025. NO MUD GAINED." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3025m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: CIRCULATED AT 250 LPM - LOSSES AT 2 M3/HR, AT 400 LPM - LOSSES AT 4 M3/HR, AT 500 LPM - LOSSES AT 13 M3/HR. 91T STRING WEIGHT DOWN, 95T STRING WEIGHT UP. BACK PRESSURE ON DP 18-30 BAR EACH TIME PUMPS SHUT DOWN. MEANWHILE CONTINUED REDUCING MUD WEIGHT FROM 1.53SG TO 1.51SG. HAVE NOW LOST 52.6 M3 MUD. MAX GAS 6%." "On 1997-11-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2584m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: SLUGGED PIPE AND BEGAN POOH TO CASING WINDOW. NORMAL DRAG." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2165m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: FINISHED POOH TO JUST ABOVE CASING WINDOW (WINDOW AT 2178M). DRAG OK. GAINED 1.1 M3 MUD." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2165m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: BROKE CIRCULATION AT 250 LPM - NO LOSSES. STAGED PUMP RATE UP TO 2000 LPM WITHOUT LOSSES. MAX GAS 17%." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2410m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: BEGAN WASHING TO BOTTOM AT 2000 LPM WHILE REDUCING MUD WEIGHT TO 1.49 SG. NO MUD LOSSES. BGG - 1.6%. TOTAL MUD LOST FOR THE DAY - 51.5 M3." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3020m. The activity was categorized as 'interruption -- lost circulation' and lasted for 7.0 hours. Operational details: CONTINUED WASHING DOWN TO 3030M. AT 3030M CIRCULATION RATE 1000 LPM, ROTARY RPM 130. LOST 1.5 M3 MUD WHILE WASHING DOWN FROM CASING WINDOW." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3030m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: GAINED 3.5 M3 WHILE MAKING CONNECTION. CLOSED IN WELL. INITIAL SICP/SIDPP 17 BAR/17 BAR. LEVELED OUT AT 20 BAR/20 BAR. TOTAL GAINED 4.5 M3." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3030m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: BLED 5 M3 MUD FROM ANNULUS THROUGH CHOKE. BLEED OFF RATE DECREASED FROM 360 LPM TO 250 LPM. CLOSED CHOKE - SICP/SIDPP 11 BAR/16 BAR. BLED OFF 2 M3 MUD FROM ANNULUS - BLEED RATE DECREASED TO 200 LPM. SICP/SIDPP 11 BAR/11 BAR. BLED REMAINING PRESSURE OFF WELL. TOTAL MUD GAINED BACK 21 M3." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3054m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: CONTINUED WASHING DOWN TO 3054M. CIRCULATED BOTTOMS UP AT 1000 LPM. NO GAINS, NO LOSSES. MAX GAS 11.5%. NO FILL." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3052m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: M/U CEMENTING STAND WHILE BOOSTING RISER. TESTED CEMENT LINE TO 100 BAR. PUMPED 4 M3 1.55 SG SPACER, 5.5 M3 1.65 SG CEMENT. DISPLACED CEMENT WITH .5 M3 SPACER AND 24 M3 MUD TO BALANCE. LOST .4 M3 MUD AND GAINED 6 BAR PRESSURE AFTER CEMENT PASSED STINGER." "On 1997-11-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2356m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: RACKED BACK CEMENT STAND AND POOH 7 STANDS DP TO 2852M - PIPE CAME OUT OF PLUG SLIGHTLY WET. PUMPED 3 M3 MUD TO CLEAR STINGER AND SLUG PIPE. CONTINUED POOH." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2223m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: FINISHED POOH TO INSIDE CASING WINDOW. NO LOSSES, NO GAINS." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2223m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: CLOSED UPR AND LINED UP HALLIBURTON. SQUEEZED 1.5 M3 MUD DOWN DRILL PIPE 100 LITERS AT A TIME, HESITATING 1 MINUTE BETWEEN PUMPING. PRESSURE AFTER STOPPING PUMP 28-30 BAR, AFTER 1 MINUTE 27-29 BAR. TOTAL MUD PUMPED DOWN DRILL PIPE 2.2 M3 (.8 M3 TO REACH LEAK OFF PRESSURE AND 1.5 M3 SQUEEZED)." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2223m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: HELD AND AND MONITORED PRESSURE ON WELL. PRESSURE DROPPED FROM 27.1 BAR TO 20.6 BAR IN 1.5 HOURS AND STABILIZED FOR .5 HOURS." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2223m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: BLED PRESSURE OFF DRILL PIPE - 0.9 M3 MUD BLED BACK. 17 BAR PRESSURE REMAINED ON ANNULUS. BLED OFF PRESSURE AND 1.1 M3. CIRCULATED BOTTOMS UP. MAX GAS 8.5%. NO GAINS, NO LOSSES - 2000 LPM CIRCULATING RATE." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2223m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: SLIPPED AND CUT DRILLING LINE." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2223m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: FINISHED SLIPPING AND CUTTING DRILLING LINE (EXTRA TIME DUE TO RECENT HIGH WINDS HAVING FOULED HANGOFF LINES IN DERRICK)." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 4.5 hours. Operational details: FINISHED POOH. CHANGED SAVER SUB ON TDS." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.5 hours. Operational details: MADE UP JET SUB, 3 STANDS HWDP, BOP TEST TOOL, AND RIH. JETTED WELLHEAD (8% MAX GAS). TESTED BOP ON BLUE POD FROM DRILL FLOOR - RAMS, FAILSAFES, AND LAP TO 35/345 BAR FOR 5/10 MINUTES, UAP TO 35/241 BAR FOR 5/10 MINUTES. FUNCTION TESTED BOP FROM TP OFFICE ON YELLOW POD. TESTED ACOUSTIC SYSTEM. POOH WITH TEST TOOL AND L/D TOOL AND JET SUB." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 150m. The activity was categorized as 'interruption -- lost circulation' and lasted for 4.5 hours. Operational details: MADE UP BIT TO MOTOR. DUMPED MEMORY AND CHANGED OUT MWD'S. SET AKO AT 1.2 DEG. AND CHECKED ALIGNMENT WITH MWD. FINISHED RIH WITH BHA." "On 1997-11-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1509m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: RIH ON DRILL PIPE. BROKE CIRCULATION EVERY 500 M." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2150m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.5 hours. Operational details: CONTINUED RIH." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2150m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP. MAX. GAS 7%. ECD AT 2000 LPM FROM ANNULAR PRESSURE SUB 1.59 SG EMW (CALCULATED 1.57 SG EMW.) ORIENTED MOTOR TO PASS THROUGH WINDOW." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2600m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: CONTINUED RIH. NO OBSTRUCTIONS IN HOLE." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2651m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: BEGAN WASHING TO BOTTOM FROM 2600 M. 1500 LPM PUMP RATE - NO LOSSES. ECD FROM ANNULAR PRESSURE SUB 1.58 SG EMW. NO GAINS, NO LOSSES OF MUD FOR THE DAY." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2920m. The activity was categorized as 'interruption -- lost circulation' and lasted for 4.0 hours. Operational details: CONTINUED WASHING DOWN FROM 2651M TO 2920M WITH 1500 LPM PUMP RATE." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2920m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: EXCESSIVE CUTTINGS AND CAVINGS AT SHAKERS. CIRCULATED UNTIL CUTTINGS VOLUME DECREASED AND ECD REDUCED FROM 1.63 SG TO 1.59 SG. CIRCULATION RATE 1500 LPM - 1000 LPM - 1500 LPM." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3054m. The activity was categorized as 'interruption -- lost circulation' and lasted for 4.5 hours. Operational details: WASHED DOWN TO 2973M. DRILLED SOFT TO FIRM CEMENT 2973M TO 3054M. CIRCULATION RATE 1500 LPM. ECD 1.59-1.60 SG. NO LOSSES." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3103m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3054M TO 3103M WHILE STAGING CIRCULATION RATE FROM 1500 LPM TO 1700 LPM. ROP CONTROLLED AT 20 MPH TO AVOID OVERLOADING ANNULUS. TOOK SPR'S." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3103m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: CUTTINGS TRANSPORT PIPE TO BAGGING STATION PLUGGED - CLEARED SAME (NOT DUE TO ANY LARGE VOLUME OF CUTTINGS AT THE TIME)." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3116m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3103M TO 3116M. CONTROLLED ROP AT 20 MPH TO AVOID OVERLOADING ANNULUS. STAGED CIRCULATION RATE UP TO 1700 LPM. ECD 1.59 SG - 1.62 SG. NO LOSSES." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3116m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: GAIN OF 0.3 M3 DETECTED - FLOWCHECKED NEGATIVE." "On 1997-11-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3125m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3116M TO 3125M." "On 1997-11-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3212m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3125M TO 3212M. INCREASED CONTROLLED ROP TO 30 MPH AND STAGED CIRCULATION RATE UP TO 2000 LPM. ECD 1.61-1.62 SG." "On 1997-11-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3268m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3212M TO 3268M AT CONTROLLED ROP OF 20-30 MPH, CIRCULATING RATE OF 2000 LPM. NO ABNORMAL TORQUE OR DRAG INDICATIONS. ECD TENDING TO INCREASE." "On 1997-11-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3268m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP AND UNTIL SHAKERS CLEANED UP AT 2000 LPM. NO LOSSES. ECD DECREASED FROM 1.62 SG TO 1.60 SG." "On 1997-11-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3272m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3268M TO 3272M." "On 1997-11-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3272m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.5 hours. Operational details: AT 3272 METERS STARTED LOSING MUD AT 20-30 M3/HR. PICKED UP FROM BOTTOM - NO UNUSUAL DRAG. REDUCED PUMP RATE TO 800 LPM. STILL LOSING MUD. QUIT CIRCULATING AND MONITORED ANNULUS ON TRIP TANK. HOLE STAYING FULL. STAGED PUMPS TO 600 LPM WHERE MUD LOSSES RESUMED. RACKED BACK 1 STAND. REDUCED RATE TO 300 LPM WITH FULL RETURNS. MIXED LCM PILL." "On 1997-11-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3248m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: WORKED STRING WITH REDUCED PUMP RATE WHILE MIXING LCM PILL. BEGAN EXPERIENCING ERRATIC TORQUE AND LOSSES OF 12 M3/HR. PICKED UP TO 3248M WHERE COMPLETE RETURNS WERE LOST AND PIPE STUCK - NO RETURNS, NO NO ROTATION, NO RECIPROCATION POSSIBLE." "On 1997-11-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 10.0 hours. Operational details: ATTEMPTED TO RIH - NO GO. JARRED DOWN WITH NO PROGRESS. JARRED AND WORKED DRILL STRING UP FROM 3248M TO 3241M. INITIALLY ATTAINED ROTATION AND A WINDOW OF A FEW METERS PIPE RECIPROCATION BUT LOST IT AGAIN. CONTINUED JARRING AND WORKING STRING. HOLE STANDING FULL - NO GAINS, NO LOSSES. ATTEMPTED CIRCULATION WITH NO SUCCESS." "On 1997-11-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: CONTINUED JARRING AND WORKING PIPE UP AND DOWN WITH NO SUCCESS. HOLE CONTINUED TO STAND FULL WITH NO GAINS OR LOSSES. MUD LOST FOR THE DAY: 55.3 M3." "On 1997-11-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 4.0 hours. Operational details: RIGGED UP ATLAS TO RUN STRINGSHOT TO BACKOFF DRILL STRING." "On 1997-11-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 11.0 hours. Operational details: FINISHED RIGGING UP ATLAS WIRELINE TO RUN BACKOFF TOOL STRING THROUGH TOP DRIVE. HAD TO RE-RIG SHEAVES BECAUSE OF HIGH DRAG ON THE LOGGING CABLE. ATLAS RIH CHECKING UP WEIGHTS EVERY 500M." "On 1997-11-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: TOP DRIVE WOULD NOT ROTATE. INVESTIGATED PROBLEM AND CORRECTED SAME." "On 1997-11-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: WORKED 32,000 FT. X LBS. AND 20 TURNS RIGHT HAND TORQUE INTO STRING. RELEASED RIGHT HAND TORQUE AND WORKED IT OUT OF DRILL STRING. DRILL STRING INADVERTENTLY BACKED OFF WHILE WORKING LEFT TURNS IN AT 25,000 FT.X LBS." "On 1997-11-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: ATLAS POOH TO 150 M JUST BELOW WELLHEAD. COLLAR LOCATOR INDICATED DRILL PIPE BACKED OFF AT 297M. SCREWED BACK INTO DRILL STRING." "On 1997-11-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: ATLAS CONTINUED POOH WITH BACKOFF TOOL STRING AND R/D SAME." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: R/U JRC SEVERENCE CHARGE ON ATLAS WIRELINE. ATLAS RIH." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3241m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: APPLIED 50 TONS OVERPULL AND 32,000 FT X LBS RIGHT TORQUE IN DP. POSITIONED 2 5/8' SEVERENCE CHARGE AT CONNECTION OF FIRST JT. OF HWDP ABOVE JAR (CHARGE WOULD NOT PASS THROUGH JAR). FIRED CHARGE - NO INDICATION AT SURFACE THAT IT FIRED, EITHER FROM ATLAS AMPMETER OR TENSION/TORQUE ON DRILL STRING. ATLAS POOH - CHARGE FOUND TO BE FIRED." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3164m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: WORKED PIPE FREE WITH 20-25K FT X LBS TORQUE AND 100 TONS OVERPULL." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3000m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: WORKED PIPE OUT OF HOLE FROM 3164M TO 3000M. ROTATING 60-100 RPM W/ 15-20K FT X LBS. OCCASIONALLY ATTEMPTED TO BREAK CIRCULATION - PARTIAL RETURNS FOR A SHORT PERIOD ONLY. PRESSURE TRAPPED ON DP WHEN PUMP SHUT DOWN. PUMPED TO FILL HOLE WHILE PULLING PIPE. COULD NOT WORK PIPE BACK DOWN HOLE." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2996m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: WORKED PIPE FROM 3000M TO 2996M. CONDITIONS DETERIORATED - NO PROGRESS FROM 2996M WITH 25K FT X LBS TORQUE AND 120 TONS OVERPULL." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2950m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: PIPE STARTED MOVING UP WITH 170 TONS OVERPULL. CONTINUED PULLING TO 2950M WHERE OVERPULL RETURNED TO NORMAL." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2164m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: PUMPED SLUG AND POOH TO ABOVE CASING WINDOW. NO LOSSES - HOLE FILL NORMAL." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2164m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: RIGGED DOWN ATLAS AND RIG SHEAVES FROM DERRICK AND TOP DRIVE. MEANWHILE CIRCULATED BOTTOMS UP AT MAXIMUM 2000 LPM - NO LOSSES. MAXIMUM GAS 40% FROM WELLHEAD AREA." "On 1997-11-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 4.0 hours. Operational details: FINISHED POOH. FOUND HWDP JOINT TO HAVE BEEN SEVERED IN THE CONNECTION AT THE TOP OF THE PIN. TOOL JOINT BELLED OUT TO OVER 8.5' (IRREGULAR OD MADE IT DIFFICULT TO GAUGE EXACTLY). LEFT IN HOLE(AS EXPECTED) -BIT STAB, NAVIDRILL, STAB, XO SUB, MWD INCLUDING MDP AND DPR SUBS, SAVER SUB, 3 X HWDP, JAR, 1 X HWDP. TOP OF FISH 3164M." "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1171m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: M/U CLEANOUT ASSEMBLY AND RIH. HOLE FILLING OK. TOTAL MUD LOST FOR THE DAY - 1.75 M3" "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2835m. The activity was categorized as 'interruption -- fish' and lasted for 4.5 hours. Operational details: CONTINUED RIH TO 2100M. CONDITIONED MUD AT 1800 LPM - FULL RETURNS. RIH TO 2600M. FILLED PIPE AND BROKE CIRCULATION. RIH TO 2835M. TOOK WEIGHT." "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2935m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: COULD NOT WORK PIPE DOWN PAST 2835M. BROKE CIRCULATION AND WASHED AND REAMED FROM 2835M TO 2935M. 1800 LPM, FULL RETURNS. EXCESSIVE CUTTINGS AT SHAKERS." "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2935m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS UP WHILE MOVING PIPE. PUMPING 1800 LPM WITH FULL RETURNS. EXCESSIVE AMOUNTS OF CUTTINGS AT SHAKERS. MAX ECD 1.65 SG. CONTINUED CIRCULATING AT 1800 LPM UNTIL ECD REDUCED TO 1.61 SG. CIRCULATED TOTAL OF 2 X BOTTOMS UP - STILL EXCESSIVE FRESH CUTTINGS." "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3161m. The activity was categorized as 'interruption -- fish' and lasted for 4.5 hours. Operational details: WASHED DOWN FROM 2935M TO TOP OF FISH AT 3161M. HIGH TORQUE IN PLACES, OTHERWISE MET LITTLE RESISTENCE. MEANWHILE RAISED MUD WEIGHT FROM 1.49 SG TO 1.52 SG. CUTTINGS/CAVINGS DECREASED. ECD INCREASED FROM 1.61 SG TO 1.64 SG. SLIGHT LOSSES - APPROX. 2 M3/HR WHILE CIRCULATING AT 1800 LPM." "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3161m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP. AT 1800 LPM SOME LOSS DETECTED - 3-6 M3/HR. ECD 1.62 - 1.64 SG. NO EXCESS CUTTINGS AT BOTTOMS UP." "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2967m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: FLOWCHECKED - SLIGHT GAIN, RATE OF GAIN FALLING. BEGAN POOH. NORMAL DRAG TO 3087M. TIGHT HOLE 3087M TO 3025M REQUIRED AS MUCH AS 50 TONS OVERPULL. TIGHT AT 3006M AND 2996M TO 2986M WHERE DRAG RETURNED TO NORMAL. HOLE DID NOT TAKE CORRECT FILL. CONT. POOH TO 2967M. BROKE CIRCULATION WITH 900 LPM, FULL RETURNS. PUMPED SLUG." "On 1997-11-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2316m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: CONTINUED POOH. NORMAL DRAG, HOLE FILL CORRECT." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 4.5 hours. Operational details: CONTINUED POOH. NORMAL DRAG, HOLE FILL CORRECT." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 315m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: BEGAN RIH WITH CEMENT STINGER TO SET SIDETRACK PLUG. TOTAL MUD LOST TODAY - 11 M3." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2826m. The activity was categorized as 'interruption -- fish' and lasted for 7.0 hours. Operational details: CONTINUED RIH WITH 3 1/2' CEMENT STINGER FROM 315M TO 2826M. BROKE CIRCULATION AND CONDITIONED MUD AT 1000M, 2100M, AND 2600M. FULL RETURNS AT 500 LPM. TOOK WEIGHT AT 2826M." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3161m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: WASHED DOWN FROM 2827M TO 2887M WITH 500 LPM AND FULL RETURNS. RIH FROM 2887M TO 3050M. WASHED DOWN FROM 3050M DUE TO BACKFLOW UP DRILL PIPE. WASHED TO 3161M WITH 500M LPM AND FULL RETURNS." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3161m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: STARTED TO CIRCULATE BOTTOMS UP FROM 3161M. EXPERIENCED LOSSES OF 6 M3/HR CIRCULATING AT 500 LPM, 2.5 M3/HR AT 350 LPM, NO LOSSES AT 250 LPM. SHUT DOWN PUMPS. SLOWLY GAINED BACK 3.8 M3. HAD LOST 16.3 M3 - NET LOSS = 12.5 M3. NO UNUSUAL HOLE DRAG EXPERIENCED." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3035m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: POOH WITH CEMENT STINGER FROM 3161M TO 3035M. STAGED PUMPS UP TO 400 LPM WITH 12 M3/HR LOSSES, 300 LPM WITH 10 M3/HR LOSSES, NO LOSSES AT 250 LPM. RIG PUMPED 5 M3 1.69 SG SPACER AT 250 LPM. NORMAL HOLE DRAG." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3035m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: LINED UP HALLIBURTON AND TESTED LINES TO 100 BAR. MIXED AND PUMPED 7.3 M3 1.95 SG CEMENT AND .9 M3 1.69 SG SPACER. LOST 1.5 M3 MUD. LINED UP RIG PUMP AND DISPLACED CEMENT TO BALANCE WITH 23.7 M3 MUD - NO RETURNS ALL PUMPING DONE AT 250 LPM UNTIL CEMENT PASSED STINGER THEN 200 LPM. GAINED 18 BAR PUMP PRESSURE AFTER CEMENT PASSED STINGER." "On 1997-12-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2560m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: STARTED POOH. GAINED MUD FROM DP AND ANNULUS - 11 M3 TOTAL - WHILE POOH TO 2560M. GAIN VERY SMALL AT 2560M. PUMPED SLUG. NORMAL HOLE DRAG" "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2106m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: CONTINUED POOH. HOLE FILL CORRECT BUT PIPE STARTED RUNNING OVER. BROKE CIRCULATION WITH 800 LPM AND FULL RETURNS. PUMPED SLUG." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: CONTINUED POOH. HOLE FILL CORRECT." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 54m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: M/U STEERABLE BHA INCLUDING LO-FLO MWD W/ ANNULAR PRESSURE SUB. MAXIMUM GAS FOR THE DAY - 18% CIRCULATING AT 2100M WHILE RIH WITH CEMENT STINGER. TOTAL MUD LOST FOR THE DAY - 28.5 M3." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: M/U AND RIH WITH 8 1/2' STEERABLE BHA. TESTED MWD. NO COMMUNICATION WITH ANNULAR PRESSURE SUB. REPLACED SUB WITH NEW ONE - STILL NO SIGNAL RIH TO 1000M." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: FILLED PIPE AND BROKE CIRCULATION WHILE STAGING PUMPS UP TO 500 LPM - FULL RETURNS." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: CONTINUED RIH WITH STEERABLE ASSEMBLY. FILLED PIPE AND BROKE CIRCULATION WHILE STAGING PUMPS UP TO 500 LPM - FULL RETURNS." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: CUT AND SLIPPED DRILLING LINE WHILE CIRCULATING 500 LPM. 1.55 SG MUD COMING OUT OF HOLE. FULL RETURNS." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: CONTINUED CIRCULATING AND STAGED PUMPS UP TO 1300 LPM. MUD WEIGHT OUT 1.65 SG MAX FROM SLUGS, MW IN 1.52 SG. NO LOSSES." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2500m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: RIH FROM 2100M TO 2500M. BROKE CIRCUALTION AT 2350M, 500 LPM, NO LOSSES." "On 1997-12-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2978m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: WASHED TO BOTTOM WITH 500 LPM AND NO LOSSES. RESISTANCE AT 2882M - 2884M REQUIRED 900 LPM TO GET THROUGH WITHOUT MOTOR STALLING. NO LOSSES. OTHERWISE NO RESISTANCE MET. VERY FINE CEMENT PARTICLES STARTED RETURNING. MUD WEIGHT INCREASED FROM 1.53 SG TO RANGE OF 1.55-1.60 SG W/ MAX. OF 1.64 SG. SOLIDS IN RETURNS UP TO 90%CEMENT." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3010m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: CONTINUED WASHING DOWN. FROM 2977M INCREASED PUMP RATE FROM 500 LPM TO 700 LPM TO MAINTAIN PROGRESS (TOP OF BALDER?). STILL A LOT OF FINE CEMENT PARTICLES COMING UP BUT NO REAL RESISTANCE. MUD WEIGHT 1.54 SG TO 1.59 SG FROM CEMENT CONTAMINATION. NO LOSSES DOWNHOLE. MAXIMUM GAS 5% (FROM WELLHEAD AREA)." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 582m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: PUMPED SLUG AND POOH. HOLE FILL OK." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: COMPLETED POOH WITH 8 1/2' SIDETRACK BHA; STOOD BACK BHA IN DERRICK." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: SERVICED RIG & TDS." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: MU 3 1/2' CMT. STINGER X 5' DP.RIH TO 1011 M & BROKE CIRCULATION. CONTINUED TO RIH TO 2100 M. BROKE CIRCULATION - EXCESSIVE AMOUNT OF CUTTINGS Ø SHAKERS - 20% CMT. IN RETURNS." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: CIRCULATED Ø 2100 M TO ACHIEVE EVEN MUD WT. & TO CLEAN SHAKERS. INCREASED CIRC. RATE TO 1300 LPM MAXIMUM - VIA STEP INCREASES. AFTER BTMS UP, SHAKERS WERE CLEAN BUT MUD WT. OUT = 1,55 SG. CONTINUED TO CIRC. UNTIL 1,52 SG MUD WT. COMING OUT. NOTE: BOOSTED RISER DURING CIRCULATING; NO MUD LOSSES DURING CIRCULATION." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2776m. The activity was categorized as 'interruption -- fish' and lasted for 4.0 hours. Operational details: MU CMT. STAND & RACKED SAME IN DERRICK. CONTINUED RIH WITH CMT.STINGER FROM 2100 - 2776 M. BROKE CIRCULATION Ø 2300, 2500 & 2700 M - FULL RETURNS Ø 500 LPM." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2776m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: WHILE TIH, TOOK 5 MT OF WEIGHT DOWN Ø 2776 M. W/R FROM 2776 - 2800 M - USING 500 LPM & 70 RPM. CONTINUED RIH TO 2980 M; BROKE CIRC. Ø 2900 M." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3004m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: WASHED DOWN LAST STAND FROM 2980 - 3004 M Ø 500 LPM; STARTED LOSING MUD Ø 4 M3/HR." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2983m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: PULLED BACK TO 3002 M; STILL LOSING MUD Ø 500 LPM. PULLED BACK TO 2983 M. BROKE CIRC. - NO MUD LOSSES Ø 200,300,400,&500 LPM. BROKE OUT CONNECTION; MUD U TBG. UP STRING." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2983m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: MU CMT. STAND & CONTINUED TO CIRCULATE. NOW LOSING MUD Ø 450 LPM BUT NO LOSSES Ø 400 LPM. CIRCULATED APPROX. 1/2 DP VOLUME WHILE PREPARING TO SPOT CMT. PLUG." "On 1997-12-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2983m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: RU CEMENT HOSE & PUMPED 5 M3 1,69 SG SPACER Ø 400 LPM USING RIG PUMP. TESTED LINES TO 125 BAR & STARTED MIXING CMT. FOR SIDETRACK PLUG." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2983m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: MIXED/PUMPED 5,4 M3 1,95 SG CMT. + 1,5 M3 1,69 SG SPACER - Ø MAXIMUM RATE OF 400 LPM. DISPLACED CMT. W/RIG PUMP-Ø 400 LPM. SLOWED RATE TO 280 LPM ONCE CMT. CLEARED END OF DP/STINGER. RECORDED 0,5 M3 OF MUD LOSS DURING THE DISPLACEMENT; NO LOSS DURING PUMPING OF CMT. SIDETRACK PLUG FROM 2983 - 2835 M. CIP Ø 0145 HRS." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2694m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: POOH TO 2694 M - TOTAL OF 10 STDS." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1100m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: PUMPED SLUG & POOH WITH CMT. STINGER." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: COMPLETED POOH WITH 3 1/2' CMT. STINGER. RACKED 3 1/2' DP IN DERRICK." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 576m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: MU 8 1/2' STEERABLE BHA & TIH TO 576 M; LD NON-OPERABLE BHI DOWNHOLE ECD SUB. TESTED MOTOR & MWD Ø 576 M." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 576m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: FUNCTION TESTED BOPS ON BOTH PODS." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2716m. The activity was categorized as 'interruption -- fish' and lasted for 4.0 hours. Operational details: CONTINUED TO RIH TO 2716 M; BROKE CIRCULATION Ø 1200 & 2105 M ON TIH." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2716m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: WHILE RIH, DRILLER RAN INTO OBSTRUCTION AT 2716M. SET DOWN 50 TON, THIS INCLUDES PARTIAL WT. OF TDS/BLOCK. PULLED FREE WITH 30TON O.PULL. STOOD BACK 1 STD. & TRIED TO ESTABLISH CIRC.BIT OR DRILLSTRING PLUGGED EVENTUALLY ABLE TO PARTIALLY/MOMENTARILY UNPLUG WITH 241 BAR BUT BIT- STRING PLUGGED AGAIN.TRIED TO BREAK PLUG W/275 BAR - UNSUCCESSFUL." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: POOH - WET - TO REPLACE BIT & MOTOR." "On 1997-12-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 23m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: PU NEW BUTTON BIT & BACK-UP MOTOR DUE TO EARLIER MISHAP. FOUND SOLIDS- 90% CMT.-PACKED IN MWD'S IN-LINE SCREEN. TESTED MOTOR & MWD - OK." "On 1997-12-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1900m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: CONTINUED TO MU & RIH WITH 8 1/2' SIDETRACK BHA - DRIFTING DP TO 2 3/4' BECAUSE OF CEMENT LOCATED IN DRILLSTRING EARLIER. BROKE CIRC. Ø 430M & Ø 1000M." "On 1997-12-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2600m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: CONTINUED TO TIH WITH SIDETRACK BHA TO 2600 M. BROKE CIRCULATION Ø 9 5/8' WINDOW." "On 1997-12-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2730m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: WASH/REAM FROM 2600 - 2730 M. HAD TO WORK THROUGH OBSTRUCTION/LEDGE Ø 2714 M." "On 1997-12-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2903m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: CONTINUED TO WASH/REAM FROM 2730 - 2903 M; TAGGED TOP OF SIDETRACK PLUG Ø 2903 M." "On 1997-12-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2911m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: DRILLED CMT. FROM 2903 - 2911 M; DRESSING-OFF SIDETRACK PLUG." "On 1997-12-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3021m. The activity was categorized as 'interruption -- fish' and lasted for 9.0 hours. Operational details: KICKED-OFF/SIDETRACKED 8 1/2' HOLE - DRILLED FROM 2911 - 3021 M. BOOSTING RISER CLEAN EVERY 3 HOURS WHILE DRILLING." "On 1997-12-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3021m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: CIRCULATED UNTIL SHAKERS CLEANED-UP; BOOSTED RISER CONSTANTLY FOR 2,5 HOURS. CAVINGS RETURNING TO SURFACE TOWARDS LAST PART OF CIRCULATION." "On 1997-12-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3042m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: DRILLED FROM 3021 - 3042 M." "On 1997-12-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3152m. The activity was categorized as 'interruption -- fish' and lasted for 11.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3042 - 3152 M. BOOSTING RISER EVERY 3 HOURS WHILE DRILLING." "On 1997-12-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3152m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: CIRC. BOTTOMS UP & BOOSTED RISER IN PREPARATION FOR TOH." "On 1997-12-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: POOH FOR BIT CHANGE. NOTE: EXCESSIVE DRAG FROM 2930 - 2825M;MAXIMUM DRAG = 30 MT/KOP=2911M." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: FINISHED POOH. BREAK-OFF BIT. CHECKED MOTOR-OK;CHECKED MWD SCREEN-OK." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2400m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: MU NEW 8 1/2' BUTTON BIT & FUNCTION TESTED MOTOR & MWD. SERVICED TDS WHILE CHECKING MOTOR/MWD'S SCRIBE LINE. COMPLETED MU BHA & RIH TO DRILL AHEAD." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2687m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: CONTINUED TO RIH WITH NEW 8 1/2' BIT TO 2687 M; TOOK 15MT WEIGHT." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3152m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: WASHED/REAMED FROM 2687 - 3152 M/TD." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'interruption -- fish' and lasted for 8.0 hours. Operational details: DRILLED 8 1/2' DIRECTIONAL HOLE FROM 3152 - 3220 M; 10 M INTO TY FORMATION. BOOSTED RISER CONSTANTLY Ø 100 SPM WHILE DRILLING. ROTATED DRILLSTRING DURING ENTIRE INTERVAL." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP IN PREPARATION FOR TOH; CONSTANTLY BOOSTING RISER - CUTTINGS STILL COMING ACROSS SHAKERS. TOOK TORQUE & WEIGHT READINGS FOR NODECO HANGER REPS." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'interruption -- well control' and lasted for 0.5 hours. Operational details: FLOW-CHECKED HOLE IN PREPARATION TO POOH - 0,95 M3 MUD BACK TO TRIP TANK IN 30 MINUTES. HOLE DIDN'T STOP FLOWING." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'interruption -- well control' and lasted for 1.5 hours. Operational details: CIRCULATED UNTIL BOTTOMS UP WAS 11,2 M3 BELOW BOPS. S/I WELL; SICP = 0 BAR AFTER 15 MINUTES. CIRCULATED BOTTOMS UP THROUGH CHOKE/CHOKE LINE Ø 400 LPM. NO GAS SEEN." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'interruption -- well control' and lasted for 1.5 hours. Operational details: OPENED WELL & CIRCULATED BOTTOMS UP AGAIN & BOOSTED RISER. NO GAS SEEN." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'interruption -- well control' and lasted for 0.5 hours. Operational details: FLOW-CHECKED; 0,50 M3 MUD BACK IN 30 MINUTES. HOLE DIDN'T STOP FLOWING. AGREED THAT HOLE MUST BE RETURNING MUD THAT WAS LOST VIA SEEPAGE." "On 1997-12-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3177m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: BACKREAMED OUT FROM 3220 - 3177 M IN PREPARATION TO RUN 7' LINER. PUMPING Ø 1650 LPM ON DRILLPIPE & 100 SPM/1400 LPM ON RISER WHILE BACKREAMING OUT AT 120 RPM." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2961m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: BACKREAMED OUT FROM 3177 - 2961 M. LOST 0,75 M3 OF MUD ON 1 STAND Ø 2961 M & SAW INCREASE IN STANDPIPE PRESSURE TREND." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2961m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP - LOST 0,95 M3 MUD WHILE CIRCULATING. CUTTINGS CONTINUE TO COME ACROSS SHAKERS." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2500m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: BACKREAMED OUT FROM 2961 - 2500 M; SAME PARAMETERS - CONSTANTLY BOOSTING RISER VIA CHOKE LINE. CUTTINGS CONTINUE TO RETURN TO SHAKERS. Ø 2615 M HAD PRESSURE INCREASE OF 10 BAR; REAMED STAND TWICE &PRESSURE RETURNED TO NORMAL. AS OF 0600 HRS. HAD LOST TOTAL OF 3,4 M3 WHILE B/R OUT & CIRCULATING." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2163m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED TO BACKREAM OUT FROM 2500 - 2210 M. PULLED THROUGH 9 5/8' WINDOW Ø 2178 - 2183 M UNTIL BIT DEPTH = 2163 M." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2163m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: CIRCULATED UNTIL SHAKERS CLEANED-UP -CIRC. Ø 1500 LPM DOWN DRILLSTRING & CONSTANTLY BOOSTING RISER Ø 3075 LPM. FLOWCHECKED HOLE BEORE POOH." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 87m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: CONTINUED TO POOH FROM 2163 - 87 M." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 87m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: DERRICKMAN ACCIDENTALLY ALLOWED 15 STANDS OF 3 1/2' DP TO BE RELEASED FROM FINGERBOARD - ACROSS DERRICK. HAD TO STOP POOH & RACK BACK THE 15 STANDS." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: FINISHED POOH WITH BHA - STANDING BACK ALL TUBULARS." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MU NODECO CEMENT HEAD & STOOD BACK IN DERRICK." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RU TO RUN 7' LINER; HELD SAFETY MEETING ON RIG FLOOR." "On 1997-12-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 571m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RAN 47 JTS. OF 7' 32 PPF L-80 NEW VAM LINER TO 571 M. FILLING LINER EVERY 5 JTS." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1094m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: CONTINUED RUNNING 7' LINER TO 1094 M; TOTAL OF 90 JTS. RAN." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1101m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MU NODECO 7' X 9 5/8' LINER HANGER INTO 7' LINER STRING." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1129m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MU 1 STD. 5' DP ONTO HANGER'S SETTING TOOL. CIRCULATED 1 LINER VOLUME." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2849m. The activity was categorized as 'drilling -- casing' and lasted for 8.5 hours. Operational details: CONTINUED TO RUN 7' LINER - ON 5' DP - FROM 1129 - 2849 M. DRIFTED DP TO 2 3/4' WHILE RUNNING; FILLED PIPE EVERY 5 STDS. BROKE CIRC. Ø 2162 M - WINDOW Ø 2178 M - WITH 380 LPM Ø 31 BAR; PU WT = 95 MT & SO WT = 77 MT Ø 2162 M. LOSING MUD WHILE RUNNING 7' LINER; TOTAL MUD LOST = 5,6 M3." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2895m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: HOLE TIGHT Ø 2849 M. WHILE TRYING TO WASH DOWN LINER Ø 270 LPM, HOLE PACKED-OFF - WITH FLOAT SHOE Ø 2895 M." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2878m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH TO 2829 M & ESTABLISHED CIRCULATION - 340 LPM Ø 38 BAR. ATTEMPTED AGAIN TO WASH LINER DOWN - HOLE PACKED-OFF AGAIN - WITH FLOAT SHOE Ø 2878 M." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2901m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: WORKED DOWN LINER-WITHOUT ROTATING-WHILE TRYING TO REGAIN CIRCULATION. HOLE PACKED-OFF AGAIN.ROTATED & WORKED DOWN-SLACKING OFF WEIGHT OF ENTIRE STRING-TO 2901 M. WHILE TRYING ESTABLISH CIRCULATION HELD 35/40 BAR BELOW 7' SHOE. MAXIMUM TORQUE UTILIZED = 24,OOO NM;PU WT=145 MT. UNABLE TO PASS 2901 M." "On 1997-12-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1830m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: POOH WITH 5' DP X 7' LINER FROM 2901 - 1830 M. HAD TO PUMP-OUT 6 STDS. OF THE FIRST 9 STDS. OUT DUE TO SWABBING; MAXIMUM PULL = 172 MT. HAD 14 MT ADDITIONAL DRAG WHILE PULLING SHOE INTO 9 5/8' WINDOW; FLOW-CHECKED Ø WINDOW FOR 15 MINUTES BEFORE CONTINUING TO POOH." "On 1997-12-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1101m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONTINUED TO POOH WITH 5' DP X 7' LINER FROM 1830 - 1101 M." "On 1997-12-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 810m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RU WEATHERFORD TONG. LD NODECO HANGER & 7' LINER. 25 JTS. OF LINER LD Ø REPORT TIME; 65 JTS. TO GO." "On 1997-12-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: CONTINUED TO POOH / LD 7' LINER FROM 810 M - SURFACE. TOTAL OF 90 JTS. LD. STOOD BACK SHOE TRACK - THREAD-LOCKED TOGETHER." "On 1997-12-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1528m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: MU 8 1/2' WIPER TRIP/STEERABLE BHA - TESTED MOTOR & MWD. TIH TO 1528M." "On 1997-12-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1528m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: LD 27 JTS. 5' DP - 21 FROM STRING & 6 FROM DERRICK - TO ALLOW STANDING BACK ADDITIONAL HWDP IN DERRICK. PU & STOOD BACK 19 JTS. 5' HWDP - FOR 7' LINER JOB." "On 1997-12-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2159m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONTINUED TO RIH TO 2159 M - ABOVE 9 5/8' WINDOW Ø 2178 M." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2159m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: S/C DRILLINE." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2746m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONTINUED TO RIH FROM 2159 - 2746M. WORKED PAST 2682M - WHERE 15 MT DRAG OCCURRED." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2894m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: CONTINUED TO TIH FROM 2746 - 2894M - WASHING & REAMING WHEN NEEDED TO PASS SEVERAL SPOTS. PROBLEMS Ø: 2746M, 2768M, 2782M, 2783 - 2793M, 2846M, 2880M, 2882M - 2894M." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2894m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: WHILE WASHING Ø 2894M, STARTED LOSING MUD AT SHAKERS BECAUSE OF LARGE AMOUNT OF CUTTINGS AT SURFACE. PU & REDUCE FLOW-RATE UNTIL SHAKERS CLEANED-UP. NOTE: CUTTINGS BACK FROM APPROX. 2800-2850M; SHAKERS WERE BLINDED-OVER BY FINE SOLIDS." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2943m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CONTINUED TO RIH - WORKING PAST TIGHT SPOTS Ø 2900M, 2914M, & 2921M." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: CONTINUED TO TIH - WASHED/REAMED FROM 2943 - 3220 M." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- casing' and lasted for 9.5 hours. Operational details: CIRCULATED - 1800 LPM Ø 200 BAR - UNTIL SHAKERS CLEANED-UP. BOOSTED RISER Ø 1500 LPM WHILE CIRCULATING DOWN DRILLSTRING. TOTAL MUD LOST = 16 M3 BUT EXCESSIVE AMOUNT OF CUTTINGS WERE CIRCULATED OUT DURING THE TIME PERIOD. FLOW-CHECKED; 0,72 M3 WERE GAINED BUT HOLE DID BECOME STATIC." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3076m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH TO 3076 M. 25 MT DRAG Ø 3090 M BUT ABLE TO WIPE THROUGH ON 2ND ATTEMPT; 30 MT DRAG Ø 3076M - UNABLE TO WIPE THROUGH AFTER 3 ATTEMPTS." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2827m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: HAD TO UTILIZE PUMP & TOP-DRIVE TO PUMP-OUT & BACKREAM-OUT FROM 3082 - 2827 M. HOLE STARTED SWABBING Ø 3028 M. LOST APPROX. 6,8 M3 MUD WHILE PUMPING-OUT & BACK-REAMING OUT," "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2827m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS-UP & BOOSTED RISER IN ATTEMPT TO CLEAN HOLE/REDUCE MUD LOSSES WHILE BACKREAMING-OUT. EXCESSIVE AMOUNT OF CUTTINGS STILL COMING ACROSS SHAKERS AFTER 1 BTMS-UP. LOST 2,2 M3 MUD WHILE CIRC. - FINAL FLOW RATE PRIOR TO STOPPING CIRC. WAS 1600 LPM Ø 155 BAR." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2711m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CONTINUED TO PUMP & B/R OUT FROM 2827 - 2711 M; HOLE SWABBING UNLESS PUMP UTILIZED. LOSING MUD WHEN PUMPING & B/R OUT; LOST 4,4 M3 MUD. NOTE: HOLE GIVING MUD BACK WHEN PUMP SHUT-DOWN." "On 1997-12-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2625m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH FROM 2711 - 2625 M; HOLE TAKING CORRECT FILL-UP WHEN PULLING STRING." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2162m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: CONTINUED TO POOH FROM 2625 - 2162 M. 30 MT DRAG Ø 2534 & 2492 M BUT ABLE TO WIPE THROUGH ON 2ND ATTEMPT THROUGH." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: FLOWCHECKED & PUMPED SLUG - BIT INSIDE OF 9 5/8' CSG. POOH FROM 2162M TO SURFACE TO CHANGE BIT & BHA." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: FINISHED POOH WITH BHA. TOTAL MUD LOSS WHILE TOH = 2,1 M3." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: MU ROTARY BHA FOR WIPER TRIP. CHANGED BHA - ADDED MWD TOOL TO BHA." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: TIH FROM 136 - 2100 M / ABOVE 9 5/8' WINDOW." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: FUNCTIONED TESTED BOPS FROM EACH POD - WEEKLY FUNCTION TEST." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: SERVICED TOP DRIVE. CHANGED-OUT SAVER SUB & INSTALLED MUD SAVER SUB ON DRILLING PUP. RACKED SAME IN DERRICK." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2100m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: REPAIRED BOLTS ON TOP DRIVE." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3206m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: CONTINUED TO RIH FROM 2100 - 3206 M / 14 M OF FILL. NOTE: TIGHT SPOTS WIPED THROUGH DURING TIH- 2740M, 2758M, 2770M, 2795M, 2850M, & 2879M. MAXIMUM WT. SLACKED-OFF = 30 MT. DID NOT CIRCULATE DURING TIH. TOTAL MUD LOSS WHILE TIH = 0,9 M3." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2172m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: POOH FROM 3206 - 2172 M / ABOVE 9 5/8' WINDOW. TIGHT SPOTS WIPED THROUGH DURING TOH: 3185M, 3053M, 2827 - 2801M, 2767M, & 2536M. MAXIMUM DRAG OVER NORMAL = 30 MT. DID NOT CIRCULATE OR ROTATE ON TOH." "On 1997-12-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2146m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: FLOWCHECKED WHILE CLEANING RIG FLOOR.PUMPED SLUG&POOH FROM 2172-2146M." "On 1997-12-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: CONTINUED TO POOH FROM 2146M TO SURFACE.TOTAL MUD LOSS WHILE TOH=,4M3." "On 1997-12-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RU TO RUN 7' LINER. HELD SAFETY MEETING. MU FLOAT SHOE TO FIRST JT.; MU FLOAT COLLAR Ø REPORT TIME." "On 1997-12-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1091m. The activity was categorized as 'drilling -- casing' and lasted for 10.5 hours. Operational details: CONTINUED RUNNING 7' 32# L-80 LINER; TOTAL OF 90 JTS/1091,52M RAN." "On 1997-12-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1103m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MU NODECO 7' X 9 5/8' LINER HANGER INTO 7' LINER STRING. LINER WT.= 38,6MT; PU WT. = 81,7MT; SO WT. = 77,1 MT." "On 1997-12-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1131m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MU 1 STD. 5' DP ONTO HANGER'S SETTING TOOL. CIRCULATED 1 LINER VOLUME; 600 LPM = 24 BAR." "On 1997-12-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2164m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: CONTINUED TO RUN 7' LINER - ON 5' DP - FROM 1131 - 2164M. DRIFTED LANDING STRING TO 2 3/4' WHILE RUNNING; FILLED PIPE EVERY 5 STDS. BROKE CIRC. Ø 2164M - WINDOW Ø 2178M - WITH 450 LPM Ø 31 BAR. PU WT. = 100 MT & SO WT. = 77 MT Ø 2164 M. MUD LOSS WHILE RUNNING LINER INSIDE OF CSG. = 2,5 M3." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2164m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: REPAIRED HYDRAULIC LEAK ON UPPER RACKING ARM - BURST SEAL FOR MAIN SHUTTLE VALVE = SOURCE OF LEAK." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2167m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: SLACKED-OFF ON LANDING STRING TO 2167 M; HAD SCR FAILURE FOR TDS, DRAWWORKS , & MUD PUMPS. ELECTRICIAN HAD TO TROUBLESHOOT PROBLEM: FOUND BURNED 'MAIN CHANGE-OVER SWITCH' - REPLACED SAME." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2593m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: CONTINUED RUNNING 7' LINER FROM 2167 - 2593 M. NOTE: WILL RUN 285 M OF 5' HWDP IN LANDING STRING." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3006m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: CONTINUED RUNNING 7' LINER FROM 2593 - 3006M. WORKED THROUGH SEVERAL TIGHT SPOTS FROM 2771 - 3006M; MAX WEIGHT SLACKED-OFF= 50 MT / MAX OVERPULL = 75 MT - ALSO USED ROTATION WHEN NEEDED/MAX TORQUE=24,4K NM." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3006m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: LOST POWER TO DRAWWORKS." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3030m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CONTINUED TO TIH WITH 7' LINER FROM 3006 - 3030 M." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3030m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: LOST POWER TO DRAWWORKS. DISCOVERED PROBLEM RELATED TO DRAWWORKS' MOTOR 'C'." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONTINUED TO TIH WITH 7' LINER FROM 3030 - 3200 M; UNABLE TO GO BELOW 3200 M." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MU CMT. STAND TO DP LANDING STRING. BROKE CIRC.; NO RETURNS. PRESSURED UP TO 131 BAR AGAINST PLUGGED BALL SEAT & SET LINER HGR. - FLOAT SHOE SPACED-OUT Ø 3198M. VERIFIED HGR. SET WITH 35 MT DOWN WT. PU 25 MT & RELEASED HGR. SETTING TOOL WITH 8 RH TURNS OF ROTATION." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RU CMT. HOSE. HELD SAFETY MEETING. PUMPED 2 M3 BASE OIL, 11,2 M3 1,60 SG SPACER 500E & 5,88 M3 1,80 SG CMT. SLURRY. (NO RETURNS WHILE PUMPING PRE-FLUSH OR CMT.)." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: DROPPED DART & DISPLACED CMT. WITH MUD Ø 450 LPM. SHEARED WIPER PLUG Ø 152 BAR; BUMPED PLUG OK. PRESSURED UP TO 180 BAR FOR 5 MINUTES. BLED OFF PRESSURE; FLOATS OK. RD CMT. HOSE. NOTE: DISPLACED WITH 38 M3 MUD; TOTAL MUD RETURNS = 5,5 M3." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2097m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: TOP OF LINER = 2097M. SLACKED-OFF 32 MT TO SET HGR. PACKER. PU & THEN ROTATED SLOWLY & SLACKED-OFF 32 MT AGAIN." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2097m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: STARTED TO PU TO PULL HGR. SETTING TOOL TO TOL/2097M. WHILE TRYING TO STAND BACK CMT. STAND, STAND 'DROPPED' ACROSS DERRICK. RECOVERED/STOOD BACK STAND." "On 1997-12-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2097m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: FINISHED PULLING HGR. SETTING TOOL TO 2097M - TOL. CIRC. BTMS UP & FLUSHED BOTH CHOKE & KILL LINES PRIOR TO TESTING TOL." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2097m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: TESTED TOL & 7' X 9 5/8' CSG. TO 180 BAR FOR 15 MIN." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1380m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: PUMPED SLUG & POOH WITH HGR. SETTING TOOL FROM 2097 -1380 M." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 765m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: CONTINUED POOH FROM 1380 - 765 M; LD 7 JTS. 5' HWDP. HAVE LD 60 JTS. 5' DP ON TOH - AS OF REPORT TIME." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: COMPLETED POOH FROM 765 M TO SURFACE; LD TOTAL OF 135 JTS. 5' DP ON TRIP OUT OF HOLE. LD NODECO LINER HANGER SETTING TOOL." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: LD NODECO CEMENT HEAD & ASSOCIATED STAND OF DP." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: LD 7' SHOETRACK - FROM FIRST ATTEMPT TO RUN LINER." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: LD 8 1/2' BHA FROM DERRICK - 2 DCS, MWD TOOL, 2 STABILIZERS & ASSOCIATED SUBS. CLEARED EXCESS HANDLING EQUIPMENT FROM RIG FLOOR." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: RIH WITH JET SUB BELOW BOP TEST TOOL. JETTED WELLHEAD FOR 15 MINUTES BEFORE LANDING TEST TOOL IN WELLHEAD." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.5 hours. Operational details: TESTED BOPS ON YELLOW POD FROM RIG FLOOR PANEL-5 MIN. LOW TEST/10 MIN. HIGH TEST: UPPER ANNULAR -20/241 BAR, LOWER ANNULAR, PIPE RAMS & FAILSAFE VALVES - 20/345 BAR. FUNCTIONED BOPS ON BLUE POD FROM TOOLPUSHER'S OFFICE MINI-PANEL. SUBSEA ENGINEER CHECKED BOPS' ACOUSTIC CONTROL SYSTEM." "On 1997-12-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 106m. The activity was categorized as 'interruption -- maintain' and lasted for 6.0 hours. Operational details: CONTINUED TO REPAIR DOLLY-TRACK SYSTEM ON UPPER RACKING ARM - HAD STARTED REPAIR WORK WHILE SIMULTANEOUSLY TESTING THE BOPS. ALSO WORKED ON TOP DRIVE'S ELECTRICAL CONTROL SYSTEM WHEN WORK ON UPPER RACKING ARM ALLOWED SAFE ACCESS TO TOP DRIVE." "On 1997-12-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 106m. The activity was categorized as 'interruption -- maintain' and lasted for 6.0 hours. Operational details: COMPLETED REPAIR TO UPPER RACKING ARM'S DOLLY-TRACK SYSTEM." "On 1997-12-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: POOH WITH BOP TEST TOOL." "On 1997-12-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: TESTED 2 TOP DRIVE SAFETY VALVES, KELLY HOSE, 2-5' KELLY COCK VALVES, 1-5' IBOP VALVE, 1-3 1/2' KELLY COCK VALVE & 1-3 1/2' IBOP VALVE TO 20/345 BAR." "On 1997-12-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: LD 1 STAND OF 5' HWDP - WITH DRIFT STUCK INSIDE PIPE. PU 4 3/4' MUD MOTOR, BROKE-OUT STABILIZER & LD MOTOR + STABILIZER." "On 1997-12-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 96m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: MU 6' BIT & ASSOCIATED ROTARY BHA TO DRILL-OUT 7' LINER SHOETRACK." "On 1997-12-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3153m. The activity was categorized as 'drilling -- trip' and lasted for 11.5 hours. Operational details: RIH WITH 6' BIT ON 3 1/2' X 5' TAPERED DRILLSTRING TO 3153 M. PU 15JTS 3 1/2' DP WHILE RIH. DRIFTED 3 1/2'-2' AND 5'-2 3/4' ON THE WAY IN. LOCATED AND WORKED PAST TOP OF LINER AT 2093M. HAD TO ROTATE BIT SLOWLY TO ENTER. RAN IN TO 3153 M." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3201m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: WASHED DOWN TO AND TAGGED WIPER PLUG AT 3167M. DRILLED SHOE TRACK AND FIRM CEMENT TO 3195M, 60-80RPM, 800LPM/100BAR. 10900-16300NM TORQUE. HAD INDICATIONS OF FLOAT COLLAR AT 3181M. CUT MW FROM 1.52 TO 1.40SG WHILE DRILLING AND CIRCULATING." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3201m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: REAMED AND CLEANED OUT RAT HOLE TO 3201M. INCREASED PUMP RATE IN STEPS TO 1300LPM. BOOSTED RISER 1340LPM." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: COMPLETED CLEANING-OUT 8 1/2' RATHOLE FROM 3201 - 3220M / TD. INCREASED FLOW RATE ON HOLE TO 1400 LPM Ø 238 BAR; BOOSTED RISER WITH 1360 LPM." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED & CONDITIONED MUD." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.5 hours. Operational details: FLOWCHECKED, PUMPED SLUG & POOH." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: MU 6' PDC BIT & 4 3/4' MOTOR. MOTOR TESTED OK. PU MWD." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: INSTALLED PROBE INTO MWD. HAD TO TROUBLESHOOT PROBLEM WITH MWD." "On 1997-12-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1236m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: COMPLETED MU 6' STEERABLE BHA. RIH ON 3 1/2' DP TO 1236 M." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1370m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONTINUED TO RIH TO 1370 M." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2073m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: PU 72 JTS. OF ADDITIONAL 3 1/2' DP WHILE TRIPPING-IN-HOLE WITH 6' BIT- TO 2073 M." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: MU 5' X 3 1/2' X/OVER WITH CIRCULATION SUB ABOVE X/OVER: CONTINUED TO RIH ON 5' DP. Ø REPORT TIME BIT DEPTH = 2400 M. HAD TO ROTATE STRING SLOWLY IN ORDER TO TRIP BIT THROUGH TOP OF LINER Ø 2097M." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2650m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONTINUED RIH WITH 5' DP TO 2650M." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2650m. The activity was categorized as 'interruption -- well control' and lasted for 0.5 hours. Operational details: OBSERVED WELL ON TRIP TANK, NO LOSSES OBSERVED." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3173m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUED RIH TO 3173M." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: PRECAUTIONARY WASHED FROM 3173M TO 3220M." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3317m. The activity was categorized as 'drilling -- drill' and lasted for 12.0 hours. Operational details: DRILLED FROM 3220M TO 3317M IN ROTATING MODE." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3317m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: TOOK MULTIPLE SURVEYS AT 3264 AND 3294M. OBTAINED INCOMPLETE SIGNALS. ALTERNATED RECEIVING FILTERS, SIGNALS STILL OUT OF SPEC. CALCULATED GOOD RESULTS FROM MULTIPLE SURVEYS AND OBTAINED GOOD SURVEYS." "On 1997-12-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3325m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: CONTINUED DRILLING FROM 3317M TO 3325M." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3348m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: CONTINUED DRILLING IN ROTATION MODE FROM 3325M TO 3348M." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3348m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: OBTAINED SURVEY AT 3321M. ATTEMPTED TO GET CONTINOUS TOOLFACE READING NO SUCCESS DUE TO MWD SIGNAL DECODING PROBLEM AT SURFACE. CHARGED RIG PUMP PULSATION DAMPERS TO 900 PSI, DID NOT GET IMPROVEMENT ON MWD SURFACE READOUT. CONTINUING TROUBLE SHOOT MWD DECODING." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3348m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: CONTINUED TROUBLE SHOOT MWD DECODING." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3360m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: CONTINUED DRILLING FROM 3348M TO 3360M. ATTEMPTED TO DRILL IN ORIENTED MODE, NO SUCCESS DUE TO WEIGHT STACKED PROBLEM AND SUBSEQUENTLY MOTOR STALLING WHEN BIT HIT FORMATION." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: BACKREAMED TO INTO 7' LINER SHOE." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BTM'S UP INSIDE LINER SHOE." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2900m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: PULLED OUT OF HOLE WITH WET PIPE." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2900m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: REPAIRED HOSE ON MUD BUCKET." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2095m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUED POOH TO TOP OF 7' LINER." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2095m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BTM'S UP. FLOW CHECKED AND PUMPED SLUG." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: CONTINUED POOH TO SURFACE." "On 1997-12-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: INSTALLED BLIND SUB AND CHANGED PROBE IN MWD. CHANGED BIT AND DUMPED MWD MEMORY." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CHECKED SCRIBE LINE. CLEANED MPR ON MWD ASSEMBLY. RESET PROBE IN ACCORDANCE TO SCRIBE LINE. LOADED MWD MEMORY." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1900m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: RIH TO 754M, BROKE CIRC AND TESTED MWD PULSES, OK. CONTINUED RIH WITH 3 1/2' DP." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3197m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: CONTINUED RIH WITH 6' DRILLING BHA TO 7' LINER SHOE." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: S/C DRILL LINE." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3360m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED RIH. PRECAUTIONARY WASH FROM 3227M TO 3360M." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3405m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: DRILLED IN ORIENTED MODE FROM 3360 - 3403M. ROTATED FROM 3403 - 3405M ATTEMPTED TO ORIENT DRILLING FROM 3405M, NO SUCCES DUE TO WEIGHT STACK UP IN STRING. NO DIFFERIENTAL PRESSURE ON BIT." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3400m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: OBTAINED 92 TON OVER PULL 3 TIMES WHEN ATTEMPTING TO PULL OFF BOTTOM AFTER ORIENTING. ESTABLISHED ROTATION AT NEUTRAL POINT. BACKREAMED AND REAMED F/3405 TO 3396M WITH MAX 2000 NM EXCESSIVE TORQUE." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3365m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: TOOK SURVEY AT 3398M. HAD 61 T OVER PULL AFTER SURVEY. BACKREAMED FROM 3398 TO 3365M." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3140m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: PULLED WITH WET PIPE FROM 3365M TO INSIDE LINER SHOE AT 3140M. HOLE IN GOOD CONDITION. TRICONE BIT REVOLUTIONS 180K, ON BTM 74K." "On 1997-12-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3140m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: PUMPED 10 MIN, FLOW CHECKED, WELL STATIC. PUMPED SLUG." "On 1997-12-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: POOH TO SURFACE. CHECKED SCRIBE LINE AND RACKED BACK MWD TOOL." "On 1997-12-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUED CHECKING THE SCRIBE LINE, DOWNLOADED MWD MEMORY. BROKE BIT." "On 1997-12-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CHANGED OUT NAVIDRILL, TESTED MOTOR. MADE UP NEW BIT." "On 1997-12-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- trip' and lasted for 8.0 hours. Operational details: MADE UP BHA AND RIH ON 3 1/2' DP AND 5' DP TO 3225M. FILLED STRING EACH 20 STANDS AND TESTED MWD ON TRIP IN." "On 1997-12-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3405m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: PRECAUTIONARY WASHED AND ROTATED FROM 3225M TO 3405M." "On 1997-12-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3432m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: DRILLED IN ROTATION MODE FROM 3405M TO 3432M." "On 1997-12-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3471m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING IN ROTATION MODE FROM 3432M TO 3471M" "On 1997-12-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3511m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: DRILLED FROM 3471M TO 3511M. REAMED EVERY STAND ONCE BEFORE CONNECTION" "On 1997-12-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3197m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: BACKREAMED FROM 3511M TO LINER SHOE. CIRCULATED 10 MIN. FLOW CHECKED" "On 1997-12-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: PUMPED SLUG AND POOH TO 2550M. HELD PIT DRILL, 3 MIN RESPONSE TIME." "On 1997-12-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: FUNCTION TESTED BOP USING YELLOW POD." "On 1997-12-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1700m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: CONTINUED POOH, RESLUGGED WHEN AT 3 1/2' DP." "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: CONTINUED POOH TO SURFACE." "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 15m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: DUMPED MEMORY IN MWD." "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CHANGED OUT NAVIDRILL AND LAID DOWN STRING STABILIZER. MADE UP SLICK NAVIDRILL AND MADE UP RR PDC BIT. CHECKED SCRIBE LINE.TESTED NAVIDRILL" "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 355m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH WITH SLICK BHA." "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3456m. The activity was categorized as 'drilling -- trip' and lasted for 6.5 hours. Operational details: CONTINUED RIH TO 3456M. FILLED PIPE EVERY 20 STANDS." "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3509m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: PRECAUTIONARY WASHED AND ROTATED FROM 3456M TO 3509M." "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3511m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: LOGGED WITH MWD FROM 3509M TO 3511 DUE TO BHA CHANGE." "On 1997-12-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3575m. The activity was categorized as 'drilling -- drill' and lasted for 10.5 hours. Operational details: DRILLED FROM 3511M TO 3575M IN ROTATIONAL MODE. REAMED EVERY STAND IN CONNECTIONS." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3588m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: CONTINUED DRILLING FROM 3575M TO 3588M." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3588m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: ATTEMPTED TO DRILL IN ORIENTED MODE, NO GO, DUE TO MOTOR STALLING WHEN BIT ENTERED BOTTOM." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3603m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: CONTINUED DRILLING IN ROTATION MODE FROM 3588M TO 3603M." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3603m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: PERFORMED SURVEY AND CONNECTION. REAMED HOLE AFTER CONNECTION DUE TO INCREASE OF TORQUE." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3603m. The activity was categorized as 'drilling -- ream' and lasted for 2.0 hours. Operational details: FOUND WASH OUT IN DRILLING PUP JT SHOULDER. RACKED BACK DRILLING STAND AND CONTINUED REAM HOLE AND OBTAINED NORMAL TORQUE THROUGH SECTION. MADE UP NEW DRILLING PUP JT." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3603m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: ATTEMPTED TO ORIENT DRILL IN ORDER TO TURN WELL TO RIGHT, NOT ABLE TO OBTAIN SLIDING CONDITIONS DUE TO STRING WEIGHT STACKED UP. 18 TON DRAG OVER NORMAL DRAG WHEN PULLED OFF BOTTOM." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 8.0 hours. Operational details: POOH WITH PUMPS AND ROTATION TO 3514M. FLOW CHECKED, WELL STATIC. PUMPED SLUG AND CONTINUED POOH. FLOW CHECKED AT LINER LAP." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: RECOVERED MWD MEMORY. CHANGED PROBE IN MWD." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CHANGED BIT, SET NAVIDRILL TO 1,5 DEGR TILT. CHECKED SCRIBELINE." "On 1997-12-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1470m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: RIH WITH DRILLING BHA TO 1470M. FILL PIPE EVERY 20 STANDS." "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2325m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: CONTINUED RIH TO 2325M." "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2325m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CHANGED TO 5' DP HANDLING EQUIPMENT. LAID DOWN WASHED DRILLING PUP JT. INSTALLED MUD SAVER." "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2325m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: CHANGED DIES ON IRON ROUGHNECK, SERVICED TOP DRIVE, RE-TIGHTED BOLTS ON STANDLIFT CYLINDER." "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3472m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: CONTINUED RIH. BROKE CIRCULATION IN LINER SHOE." "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3603m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: PRECAUTIONARY WASHED AND ROTATED FROM 3514M TO 3603M." "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3656m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: DRILLED AND ORIENTED FROM 3603M TO 3656M. REAMED EVERY STAND IN CONN" "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3656m. The activity was categorized as 'drilling -- ream' and lasted for 2.0 hours. Operational details: REAMED SECTION 3642 TO 3637M AND 3625 TO 3615M DUE TO TIGHT HOLE." "On 1997-12-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: PUMPED SLUG AND POOH TO LINER SHOE. FLOW CHECKED, WELL STATIC. CONTINUED POOH TO 2400M. RE-SLUGGED AT 2765M." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: CONTINUED POOH TO SURFACE." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: RECOVERED MWD MEMORY." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: LAID DOWN BIT AND FOUND TIP OF CONE NO 3 MISSING. SET NAVIDRILL TO 0,8 DEGR TILT AND CHECK SCRIBE LINE." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3571m. The activity was categorized as 'drilling -- trip' and lasted for 8.0 hours. Operational details: CONTINUED M/UP BHA AND RIH TO 3571M. FILLED STRING EVERY 20 STAND." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3656m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: PRECAUTIONARY WASH AND ROTATE FROM 3571M TO 3656. WASHED ONTO BTM SEVERAL TIMES PRIOR TO DRILLING." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3690m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED IN ROTATION MODE FROM 3656M TO 3690M. WASHED TO BTM AFTER CONNECTIONS. NOT ABLE TO DECODE MWD SIGNALS. SIGNALS MISSING OR TO WEAK AT SURFACE." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3570m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: REAMED SECTION FROM 3690M TO 3570M 3 TIMES." "On 1997-12-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3350m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: PUMPED SLUG AND POOH TO 3350M. HOLE IN GOOD CONDITION." "On 1997-12-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 40m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: CONTINUED POOH. RE-SLUGGED AT LINER SHOE." "On 1997-12-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 7.0 hours. Operational details: BROKE OUT BIT. DUMP MWD MEMORY, CHANGED PROBE IN MWD. LAID DOWN MPR AND SERVICED SAME. MADE UP MPR AND MWD ASSY. CHECKED MWD CONNECTOR." "On 1997-12-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'interruption -- repair' and lasted for 7.0 hours. Operational details: MADE UP BIT AND CHECKED SCRIBE LINE. RIH TO LINER SHOE. FILLED STRING EVERY 20 STANDS." "On 1997-12-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: S/C DRILLING LINE." "On 1997-12-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3645m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: CONTINUED RIH TO 3629M. BROKE CIRCULATION AND WASH AND ROTATED F/3629- 3645M." "On 1997-12-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3679m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: LOG SECTION FROM 3645M TO 3679M WITH MWD. OBSERVED PIT GAIN 0,5 M3." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3669m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: PERFORMED FLOW CHECK AND OBSERVED WELL FLOW. CLOSE ANNULAR, NO PRESSURE OBSERVED. OPENED CHOKE AND OBSERVED WELL STATIC. FOUND MUD WEIGHT TO BE INSUFFICIENT AND CAUSED U TUBE EFFECT. CORRECTED MUD WEIGHT IN ACTIVE FROM 1.45 SG TO 1.40 SG WHILST RECIPROCATED STRING AND CIRCULATED WITH 20 SPM." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3690m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: CONTINUED LOGGING WITH MWD FROM 3679M TO 3690M. MADE 4 ATTEMPTS BEFORE OBTAINED GOOD SURVEY. WASHED ONTO BTM SEVERAL TIMES PRIOR TO DRILLING." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3708m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: DRILLED FROM 3690M TO 3708M." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3717m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: DRILLED FROM 3708M TO 3717M. ROP GRADUALLY DECREASED TO ZERO FOR 1 HRS" "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3690m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: REAMED SECTION FROM 3717M TO 3690M." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 9.0 hours. Operational details: POOH TO LINER SHOE. FLOW CHECKED AND PUMPED SLUG. CONTINUED POOH TO SURFACE AND CHANGED AKO MOTOR AND BIT." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: MADE UP 5 7/8' STABILIZER ON TOP OF AKO AND SET AKO TO 0 DEGR. CHECKED SCRIBE LINE." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: DUMPED MWD MEMORY." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1837m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: RIH TO 1837M. FILLED PIPE EACH 35 STANDS. TESTED MWD OK AT 1000M." "On 1997-12-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1873m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: DISCOVERED SMOKE FROM INSIDE DRAWORKS. FOUND SMOULDERS FROM GREASE/OBM BEHIND BRAKE BANDS. EXTINGUISED SMOULDERS AND CLEANED BRAKE BANDS." "On 1997-12-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3661m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONTINUED RIH TO 3661M. CHECKED NEW BHA IN HOLE BY PULLING 15M UP ON EACH STAND FROM TOP OF CHALK FORMATIONS." "On 1997-12-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3717m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: WASHED AND REAMED TO 3716M." "On 1997-12-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3728m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: WASHED ONTO BTM 2 TIMES PRIOR TO DRILLING AND DRILLED FROM 3717M TO 3728M." "On 1997-12-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3887m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED FROM 3728M TO 3887M. REAMED EACH STAND PRIOR TO CONNECTION SURVEYS." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3950m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING FROM 3887M TO 3950M." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3959m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: DRILLED FROM 3950M TO 3959M. ERRATIC DECODING FROM MWD FROM 3950M." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3959m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 1.5 hours. Operational details: CIRCULATED DRILLING BREAK FOR GEOLOGICAL SAMPLES." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3968m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED FROM 3959M TO 3968M." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3968m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 1.5 hours. Operational details: CIRCULATED DRILLING BREAK FOR GEOLOGICAL SAMPLES." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3982m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: DRILLED FROM 3968M TO 3982M." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3982m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 2.0 hours. Operational details: CIRCULATED DRILLING BREAK FOR GEOLOGICAL SAMPLES." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4031m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: CONTINUED DRILLING FROM 3982M TO 4031M." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4031m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 1.5 hours. Operational details: CIRCULATED FOR GEOLOGICAL SAMPLES. SAND IN SAMPLES AND SMALL SHOWS." "On 1997-12-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3970m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: PRECATIONARY PUMPED OUT OF HOLE TO 3970M." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3717m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUED PUMPING OUT OF HOLE TO 3717M." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3717m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED ANNULUS CONTENT FROM 3717M TO TOL." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONTINUED POOH WET TO LINER SHOE." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3198m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED AT LINER SHOE AND BOOSTED RISER UNTIL SHAKERS CLEANED UP AT 1,6 TIMES RISER CONTENT. FLOW CHECKED, WELL STATIC. PUMPED SLUG." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2123m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED POOH." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONTINUED POOH WITH DRILLING BHA FOR CORING." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: LAID DOWN MWD PROBE, MWD, BIT AND AKO MOTOR." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: MADE UP WELLHEAD JETTING SUB. RIH AND WASHED WELLHEAD AREA." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: MADE UP BOP TEST TOOL ON TOP OF WASH STRING. RIH AND SET TEST PLUG IN WELLHEAD." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: TESTED BOP ON BLUE POD FROM RIG FLOOR PANEL: 5-MIN LOW/ 10-MIN HIGH TEST: UPPER ANNULAR 20/241 BAR, LOWER ANNULAR, PIPE RAMS & FAILSAFE VALVES - 20/345 BAR. FUNCTIONED BOPS ON YELLOW POD FROM TOOLPUSHER'S OFFICE MINI-PANEL." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: POOH AND LAID DOWN TEST PLUG AND JETTING SUB ASSY." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: TESTED LOWER AND UPPER IBOP, ROTARY HOSE 5/10 MIN, 35 BAR/345 BAR, OK." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: DISCONNECTED TEST HOSE AND PICKED UP AKO MOTOR. BROKE DOWN X/OVER FROM AKO MOTOR. LAID DOWN AKO MOTOR." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: MADE UP 20,5M COREBARREL." "On 1997-12-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 680m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: MADE UP AND DRIFTED BHA. RIH TO 680M. DRIFTED ALL PIPE TO 2'" "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3508m. The activity was categorized as 'formation evaluation -- trip' and lasted for 5.5 hours. Operational details: CONTINUED RIH WITH COREBARREL. FILL PIPE EACH 1000 M. 15T RESISTANCE AND 25T OVERPULL AT 3508M." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3514m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: BROKE CIRCULATION AND REAMED WITH 110 RPM AND 575L/ MIN FROM 3508M TO CURRENT DEPTH 3514M." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3680m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: RIH FROM 3514M TO 3680M - TOOK WEIGHT." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3772m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: REAMED TIGHT HOLE FROM 3680M TO 3772M." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3772m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: WORKED TIGHT HOLE AT 3772M. MAX O'PULL 70 TONS." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3824m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: CONTINUED REAMING FROM 3772M TO 3824M. STRING STUCK AT 3824M BIT DEPTH" "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3824m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: JARRED PIPE FREE - MAX O'PULL 75 TONS." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 8.5 hours. Operational details: POOH WET TO 3563M. SLUGGED PIPE, FLOWCHECKED AND CONTINUED POOH. FLOW CHECKED AT SHOE. FINISHED POOH. RACKED CORE BARREL IN DERRICK." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: P/U NEW ROTARY DRILLING ASSEMBLY INCLUDING MWD AND 3 X 4 3/4' DC'S. WEATHER CONDITIONS DETERIORATING - RACKED ABOVE BACK IN DERRICK." "On 1998-01-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: SUSPENDED OPERATIONS DUE TO HIGH WINDS AND SEA STATE. WIND 25-30 M/S, SEAS 5M AND RISING, ROLL 3-4 DEG. WITH PEAKS OF 6 DEG., PITCH 1-3 DEG, HEAVE 2M AND RISING, RISER ANGLE 2-4 DEGREES." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: W.O.W. MAX WIND 34 M/S, MAX PITCH 2 DEG, MAX ROLL 5 DEG, MAX HEAVE 7.8M." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3341m. The activity was categorized as 'drilling -- trip' and lasted for 9.5 hours. Operational details: WEATHER CONDITIONS OK TO RESUME OPERATIONS. INSTALLED PROBE AND MEMORY IN MWD. RIH FILLING PIPE EVERY 1000M. BROKE CIRCULATION AT SHOE AND CIRCULATED UNTIL GAS < 5%. CONTINUED RIH TO 3341M - TOOK WEIGHT." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3361m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: REAMED FROM 3341M TO 3361M (SHALE STRINGERS)." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3571m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONTINUED RIH TO 3571M - TOOK WEIGHT." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3595m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: REAMED FROM 3571M TO 3595M (TOP OF HOD FORMATION - ALSO HAD DRILLED ORIENTING THROUGH THIS INTERVAL)." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONTINUED RIH TO 3660M - TOOK WEIGHT." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3738m. The activity was categorized as 'drilling -- ream' and lasted for 2.0 hours. Operational details: REAMED FROM 3660M TO 3738M." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3790m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONTINUED RIH TO 3790M - TOOK WEIGHT." "On 1998-01-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3860m. The activity was categorized as 'drilling -- ream' and lasted for 4.0 hours. Operational details: REAMED HOLE FROM 3790M TO 3860M." "On 1998-01-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3960m. The activity was categorized as 'drilling -- ream' and lasted for 6.0 hours. Operational details: CONTINUED REAMING HOLE FROM 3860M TO 3960M. HOLE IS TIGHT IN SHORT, DISCREET INTERVALS THAT TEND TO STALL ROTARY. WORST PLACES HAVE BEEN AT 3790M AND 3835M TO 3846M. AFTER REAMING THROUGH EACH PLACE ONCE IT IS CLEAR AND FREE." "On 1998-01-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4031m. The activity was categorized as 'drilling -- ream' and lasted for 8.5 hours. Operational details: CONTINUED REAMING FROM 3960M TO 4031M. AS BEFORE, HOLE WAS TIGHT IN SHORT DISCREET INTERVALS THAT CLEARED UP AFTER REAMING THROUGH ONCE." "On 1998-01-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4037m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED 6' HOLE FROM 4031M TO 4037M. FROM 4036M - 4037M ROTARY WAS STALLING OUT. AT 4037M PUMP PRESSURE DROPPED 4-5 BAR, ROTARY TORQUE SMOOTHED OUT AND NO PROGRESS WAS MADE FOR APPROX. 1 HOUR." "On 1998-01-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4037m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS UP FOR SAMPLES." "On 1998-01-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2373m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: POOH 10 STANDS - NO UNUSUAL DRAG. PUMPED SLUG AND CONTINUED POOH. 20 TONS OVERPULL AT 3530M OTHERWISE HOLE IN GOOD SHAPE." "On 1998-01-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: CONTINUED POOH TO P/U CORE BARREL. DUMPED MWD MEMEORY AND RACKED BACK BHA." "On 1998-01-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: FINISHED L/D MWD AND RACKING BACK ROTARY ASSEMBLY." "On 1998-01-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: P/U CORE BARREL FROM DERRICK AND CHANGED OUT STABILIZERS FROM 5 31/32' TO 5 27/32'. M/U CORE HEAD." "On 1998-01-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3996m. The activity was categorized as 'formation evaluation -- trip' and lasted for 9.5 hours. Operational details: RIH WITH CORE BARREL TO CUT CORE #1. FILLED PIPE EVERY 1000M, BROKE CIRCULATION AT CASING SHOE. NO RESISTENCE MET WHILE RIH." "On 1998-01-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4037m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: WASHED TO BOTTOM FROM 3996M TO 4037M - NO FILL. DROPPED BALL AND TOOK SPR'S. ATTEMPTED TO START CORING - STRING STUCK ON BOTTOM FOR 20 MINUTES - JARRED REPEATEDLY TO FREE." "On 1998-01-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4048m. The activity was categorized as 'formation evaluation -- core' and lasted for 2.5 hours. Operational details: CUT CORE #1 FROM 4037M TO 4048M. ROTARY VERY SENSITIVE TO BIT WEIGHT. RAN ONLY 0-2 TONS WOB TO AVOID STALLING DRILL STRING AND HAVING TO PICK UP OFF BOTTOM TO RESTART ROTATION." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4054m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.0 hours. Operational details: CONTINUED CUTTING CORE #1 FROM 4048M TO 3054.5M. ROP AND TORQUE INDICATED POSSIBLE JAMMED BARREL." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3842m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: FLOWCHECKED, PUMPED SLUG AND POOH." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3842m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: REPAIRED IRON ROUGHNECK - SHEARED BOLTS ON TORQUE WRENCH." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2004m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.5 hours. Operational details: CONTINUED POOH WITH CORE #1. NORMAL DRAG ALL THE WAY OUT." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 5.0 hours. Operational details: FINISHED POOH WITH CORE #1. POOH 5 MIN/STAND FOR LAST 400M." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: L/D CORE #1. RECOVERED 12.8M OF 17.5M CUT (73%)." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: CUT AND SLIPPED DRILLING LINE." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: REDRESSED CORE BARREL." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4023m. The activity was categorized as 'formation evaluation -- trip' and lasted for 9.5 hours. Operational details: RIH WITH CORE BARREL. FILLED PIPE EVERY 1000M. BROKE CIRCULATION AT 2000M AND CIRCULATED 36% MAXIMUM GAS UP FROM WELLHEAD. NO RESISTANCE MET WHILE RIH." "On 1998-01-05, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4054m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: WASHED TO BOTTOM FROM 4023M TO 4054M - NO FILL." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4054m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: DROPPED BALL AND TOOK SPR'S." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4070m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.0 hours. Operational details: CUT CORE #2 FROM 4054,5M TO 4070,5M. TORQUE SMOOTHED OUT, ROP DROPPED TO 0, PUMP PRESSURE DECREASED 10 BAR - BARREL JAMMED." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2069m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.5 hours. Operational details: FLOWCHECKED, PUMPED SLUG AND POOH. NORMAL DRAG." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.5 hours. Operational details: FINISHED POOH WITH CORE #2. POOH AT REDUCED SPEED FOR LAST 400M." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: L/D CORE #2. RECOVERED 17,3M. CORRECTED TD TO 4072M MD. 100% RECOVERY." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: SERVICED TOP DRIVE." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: REDRESSED CORE BARREL." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4063m. The activity was categorized as 'formation evaluation -- trip' and lasted for 8.0 hours. Operational details: RIH WITH CORE BARREL. FILLED PIPE EVERY 1000M. NO RESISTANCE MET WHILE RIH TO 4063M." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4072m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: WASHED TO BOTTOM FROM 4063M TO 4072M - NO FILL. DROPPED BALL AND TOOK SPR'S." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4090m. The activity was categorized as 'formation evaluation -- core' and lasted for 2.5 hours. Operational details: CUT CORE #3 FROM 4072M TO 4090,5M. BARREL FULL. OCCASIONAL HARD STRINGERS." "On 1998-01-06, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4085m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: FLOWCHECKED AND PUMPED SLUG." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 212m. The activity was categorized as 'formation evaluation -- trip' and lasted for 6.0 hours. Operational details: POOH WITH CORE #3. NORMAL DRAG." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: FINISHED POOH WITH CORE #3. POOH AT REDUCED SPEED FOR LAST 400M." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: L/D CORE #3. RECOVERED 18M." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: REDRESSED CORE BARREL." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: SERVICED RIG AND TOP DRIVE." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4054m. The activity was categorized as 'formation evaluation -- trip' and lasted for 8.0 hours. Operational details: RIH WITH CORE BARREL TO 4054M. FILLED PIPE EVERY 1000M. NO RESISTANCE MET WHILE RIH." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4090m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: WASHED TO BOTTOM FROM 4054M TO 4090M. NO FILL. DROPPED BALL AND TOOK SPR'S." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4109m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.0 hours. Operational details: CUT CORE #4 FROM 4090M TO 4109M. CORE BARREL FULL." "On 1998-01-07, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2179m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.5 hours. Operational details: FLOWCHECKED AND PUMPED SLUG. POOH WITH CORE #4. TIGHT IN PLACES FROM 4090M TO 4062M (35 TONS MAX OVERPULL)." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 4.5 hours. Operational details: FINISHED POOH WITH CORE #4. POOH AT REDUCED SPEED FOR LAST 400M." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: L/D CORE #4. RECOVERED 19M. RACKED BACK CORE BARREL." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: BEGIN PICKING UP DRILLING ASSEMBLY WITH STRAIGHT MOTOR." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 34m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: M/U 6' DRILLING ASSEMBLY INCLUDING STRAIGHT MOTOR AND MWD." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3190m. The activity was categorized as 'drilling -- trip' and lasted for 6.5 hours. Operational details: RIH TO 7' SHOE. FILLED PIPE EVERY 1000M." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3190m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: FUNCTION TESTED BOP FROM MAIN PANEL ON BLUE POD." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4007m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUED RIH TO 4007M. MET NO RESISTANCE." "On 1998-01-08, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4096m. The activity was categorized as 'formation evaluation -- log' and lasted for 7.5 hours. Operational details: REAMED FROM 4007M TO 4096M TO OBTAIN MWD LOG. HIGH TORQUE LIMITED PROGRESS." "On 1998-01-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4109m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: FINISHED REAMING TO BOTTOM TO OBTAIN MWD LOG. HIGH TORQUE LIMITED PROGRESS. NO FILL." "On 1998-01-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4139m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED 6' HOLE FROM 4109M TO 4139M. MWD SIGNAL INTERMITTENT AFTER DRILLING STARTED RESULTING IN POOR LOG QUALITY." "On 1998-01-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4130m. The activity was categorized as 'formation evaluation -- other' and lasted for 2.5 hours. Operational details: POOH TO 4105M. STRING STUCK BRIEFLY AT 4123M WHILE RACKING BACK STAND OF DRILL PIPE. REAMED FROM 4105M TO 4130M TO ACQUIRE BETTER MWD LOG." "On 1998-01-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4139m. The activity was categorized as 'formation evaluation -- other' and lasted for 1.0 hours. Operational details: FINISHED REAMING FROM 4130M TO 4139M TO ACQUIRE BETTER MWD LOG." "On 1998-01-09, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4248m. The activity was categorized as 'drilling -- drill' and lasted for 17.0 hours. Operational details: DRILLED 6' HOLE FROM 4139M TO 4248M." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED 6' HOLE FROM 4248M TO T.D. AT 4250M." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS UP AND BOOSTED RISER - SHAKERS CLEAN." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4094m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: POOH. 20-30 TONS MAXIMUM OVERPULL ABOVE NORMAL DRAG. AFTER SETTING SETTING BACK STAND AT 4075M HOLE WAS TIGHT - 60 TONS OVERPULL. P/U STAND, M/U TOP DRIVE, BROKE CIRCULATION AND WASHED AND REAMED TO 4094M. AFTER BREAKING AND LAYING OUT SINGLE PIPE WAS FOUND TO BE TO BE STUCK AT 4094M." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: WORKED AND JARRED ON STUCK PIPE. NO PROGRESS. GOOD CIRCULATION." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: WORKED STUCK PIPE FREE." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4084m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: REAMED AND BACKREAMED FROM 4109M TO 4084M." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 10.5 hours. Operational details: POOH TO 4017M. PUMPED SLUG AND CONTINUED POOH TO RUN LOGS. L/D MWD, MOTOR AND JAR." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: R/U ATLAS C/W COMPENSATING EQUIPMENT TO RUN WIRELINE LOGS." "On 1998-01-10, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3000m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.0 hours. Operational details: ATLAS RAN MAC/GR FROM 7' CASING SHOE AT 3198M." "On 1998-01-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.5 hours. Operational details: ATLAS FINISHED RUNNING MAC/GR. R/D LOGGING TOOL. AT 3200M TOOL WT. + LINE WT = 4000 LBS. PICKUP WEIGHT WAS 7000 LBS." "On 1998-01-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2000m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: R/U AND RUN VSP." "On 1998-01-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.0 hours. Operational details: FINISHED RUNNING VSP IN CASING. R/D ATLAS." "On 1998-01-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 210m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: M/U BHA FOR WIPER TRIP AND RIH." "On 1998-01-11, at Well NO 15/9-19 B, a drilling event occurred at a depth of 210m. The activity was categorized as 'interruption -- maintain' and lasted for 10.0 hours. Operational details: INVESTIGATED HYDRAULIC LEAK ON TOP DRIVE. DURING INSPECTION FOUND FOUR BROKEN BOLTS ON TOP DRIVE MOTOR TRUNNION, MAIN ELECTRIC MOTOR LOOSE, LUBE OIL PUMP LOOSE, AIR DISTRIBUTION MANIFOLD LOOSE, AND SEVERAL BROKEN FITTINGS. BEGAN REPAIRING SAME." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 210m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: FINISHED REPAIRING TOP DRIVE." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1827m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.0 hours. Operational details: CONTINUED RIH FOR WIPER TRIP." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2760m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: CONTINUED RIH FOR WIPER TRIP. LOST ELECTRIC POWER TO DRAWWORKS." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3760m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: RESTORED ELECTRIC POWER TO DRAWWORKS." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: CONTINUED RIH FOR WIPER TRIP TO 7' CASING SHOE." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: CUT AND SLIPPED DRILLING LINE." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4137m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: FINSHED RIH FOR WIPER TRIP. STOOD UP AT 4137M WITH 15 TONS." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: WASHED AND REAMED FROM 4112M TO BOTTOM AT 4250M - 3 METERS FILL." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS UP AND BOOSTED RISER." "On 1998-01-12, at Well NO 15/9-19 B, a drilling event occurred at a depth of 988m. The activity was categorized as 'formation evaluation -- trip' and lasted for 7.5 hours. Operational details: FLOWCHECKED, PUMPED SLUG, AND POOH TO RUN LOGS ON DRILL PIPE - NORMAL DRAG." "On 1998-01-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: FINISHED POOH TO RUN LOGS ON DRILL PIPE." "On 1998-01-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: SERVICED TOP DRIVE AND CLEANED RIG FLOOR" "On 1998-01-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 117m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: R/U ATLAS TLC EQUIPMENT AND VSP/SUPERCOMBO LOGGING TOOL STRING AND BEGAN RIH." "On 1998-01-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3174m. The activity was categorized as 'formation evaluation -- log' and lasted for 10.5 hours. Operational details: CONTINUED RIH WITH VSP/SUPER COMBO LOGGING TOOLS ON DRILL PIPE TO JUST ABOVE 7' CASING SHOE." "On 1998-01-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3174m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: INSTALLED SIDE ENTRY SUB. R/U ATLAS SHEAVES IN DERRICK. ATLAS RIH WITH WET CONNECTOR WHILE RIG SIMULTANEOUSLY PUMPED AT 400 LPM AND 40 BAR. ATLAS LATCHED WET CONNECTOR AND CHECKED LOGGING TOOLS AND TELEMETRY. TIGHTENED SIDE ENTRY SUB PACKOFF BUSHING AND PULL TESTED.." "On 1998-01-13, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4240m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.0 hours. Operational details: CONTINUED RIH WITH LOGGING TOOLS ON DRILL PIPE. LOGGED MAC WHILE GOING DOWN. NO RESISTENCE MET EXCEPT FOR ONE SLIGHT FLICKER AT 4147M." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3861m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: POOH WITH VSP/SUPER COMBO LOGGING TOOLS ON DRILL PIPE. RAN VSP WHILE POOH. NORMAL DRAG." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3861m. The activity was categorized as 'formation evaluation -- other' and lasted for 1.0 hours. Operational details: RADIO COMMUNICATIONS WITH VSP BOAT FAILED AND REQUIRED BOAT TO RETURN TO RIG TO DROP OFF ANOTHER RADIO." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3619m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: CONTINUED LOGGING 6' HOLE WITH VSP." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3184m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.0 hours. Operational details: FINISHED LOGGING 6' HOLE WITH VSP ON DRILL PIPE." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4240m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.5 hours. Operational details: RAN BACK IN HOLE WITH VSP/SUPERCOMBO LOGGING TOOL STRING ON DRILL PIPE. NO RESISTANCE." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3191m. The activity was categorized as 'formation evaluation -- log' and lasted for 8.0 hours. Operational details: POOH LOGGING 6' HOLE WITH DENSITY/NEUTRON TOOLS ON DRILL PIPE. NORMAL DRAG." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3191m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: ATLAS PULLED WET CONNECTOR LOOSE - REQUIRED +\- 1/2 HOUR WORKING WIRELINE TO 9000 LBS (MAXIMUM PULL BEFORE LINE ON DRUM POSSIBLY CRUSHING) AND FINALLY RECIPROCATING DRILL STRING. ATLAS POOH WITH WIRE LINE. REMOVED WET CONNECTOR AND SIDE ENTRY SUB FROM STRING. R/D ATLAS SHEAVES FROM DERRICK." "On 1998-01-14, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3163m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: PUMPED SLUG AND POOH WITH VSP/SUPERCOMBO LOGGING TOOLS ON DRILL PIPE." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.0 hours. Operational details: CONTINUED POOH WITH LOGGING TOOLS ON DRILL PIPE. L/D LOGGING TOOLS FROM FIRST RUN ON DRILL PIPE INCLUDING VSP, MAC, NEUTRON, DENSITY." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: COMPLETED LD VSP/SUPERCOMBO LOGGING TOOLSTRING." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3171m. The activity was categorized as 'formation evaluation -- log' and lasted for 9.5 hours. Operational details: RIH WITH FMT TOOLSTRING ON DRILLPIPE - TO JUST ABOVE 7' SHOE." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3171m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: INSTALLED SIDE ENTRY SUB INTO STRING. RU ATLAS SHEAVES IN DERRICK. ATLAS RIH WITH WET CONNECTOR WHILE PUMPING 400 LPM Ø 45 BAR. ATLAS LATCHED WET CONNECTOR." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3171m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: CONTINUED TO CIRCULATE 680 LPM Ø 76 BAR DUE TO HIGH GAS LEVEL - MAXIMUM READING OF 18%." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3171m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: MUD U-TUBING OUT OF DRILLPIPE AT HIGH RATE. CIRCULATED BOTTOMS-UP 1100 LPM Ø 120 BAR IN ORDER TO BALANCE MUD SO THAT TRIPPING COULD CONTINUE." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3171m. The activity was categorized as 'formation evaluation -- other' and lasted for 1.5 hours. Operational details: NOTICED WASH-OUT ON SIDE ENTRY SUB'S PACKING NUT. REMOVED NUT; RUBBER PACKING NOT IN PLACE. REALIZED THAT SIDE ENTRY SUB'S PROFILE WAS ALSO WASHED. INSTALLED A NEW RUBBER PACKING; UNSUCCESSFUL IN TIGHTENING PACKING NUT COMPLETELY - DUE TO WASH-OUT. DETERMINATION MADE THAT SIDE ENTRY SUB REQUIRED REPLACING." "On 1998-01-15, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3171m. The activity was categorized as 'formation evaluation -- other' and lasted for 3.0 hours. Operational details: ATLAS PULLED WET CONNECTOR LOOSE - REQUIRED 65 MINUTES OF CONSTANT PULLING & WORKING ELECTRIC LINE & RECIPROCATING DRILLPIPE. FINALLY PULLED WET CONNECTOR FREE AFTER USING A MAXIMUM OF 11300 LBS- 5 MT - OF PULL. ATLAS POOH WITH ELECTRIC LINE;NOTICED A DAMAGED SECTION-2 CM LONG-OF WIRELINE WHEN THEY STARTED POOH. START RD SIDE ENTRY SUB." "On 1998-01-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3172m. The activity was categorized as 'formation evaluation -- other' and lasted for 1.0 hours. Operational details: COMPLETED RD SIDE ENTRY SUB FROM DRILLPIPE." "On 1998-01-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3172m. The activity was categorized as 'formation evaluation -- other' and lasted for 4.5 hours. Operational details: REPLACED DAMAGED DRUM OF ATLAS ELECTRIC LINE. MUD STILL OUT OF BALANCE - CIRCULATED FROM 0100 HRS. - 0430 HRS. - 950 LPM Ø 160 BAR - TO BALANCE OUT MUD/2 BOTTOMS-UP CIRCULATED." "On 1998-01-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3172m. The activity was categorized as 'formation evaluation -- other' and lasted for 0.5 hours. Operational details: STARTED RU ELECTRIC LINE INTO SHEAVES BEFORE MU REPLACEMENT SIDE ENTRY SUB INTO DRILLPIPE." "On 1998-01-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3172m. The activity was categorized as 'formation evaluation -- other' and lasted for 3.0 hours. Operational details: COMPLETED MU REPLACEMENT SIDE ENTRY SUB INTO STRING. ATLAS RIH WITH WET CONNECTOR ON ELECTRIC LINE WHILE PUMPING. ATLAS LATCHED WET CONNECTOR WHILE PUMPING 800 LPM Ø 138 BAR." "On 1998-01-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4200m. The activity was categorized as 'formation evaluation -- log' and lasted for 9.0 hours. Operational details: RIH WITH FMT TOOLSTRING ON DRILLPIPE - TAKING PRESSURE READINGS FROM 3223 M TO 4200 M. 30 ATTEMPTED PRESSURE READINGS; 22 SUCCESSFUL. ATTEMPTED TO TAKE SAMPLE Ø 4109 M - UNSUCCESSFUL - LOST SEAL." "On 1998-01-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3173m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: POOH WITH FMT TOOLSTRING/DRILLPIPE FROM 4200 M TO 3173 M - PLACING SIDE ENTRY SUB Ø RIG FLOOR." "On 1998-01-16, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3173m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: ATLAS PULLED WET CONNECTOR LOOSE WITH NO PROBLEMS; MAXIMUM OF 6000 LBS - 2,7 MT - OF PULL NEEDED. ATLAS POOH WITH THE ELECTRIC LINE. RD SIDE ENTRY SUB FROM DRILLPIPE STRING." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1734m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.0 hours. Operational details: POOH WITH FMT TOOLSTRING FROM 3173 - 1734 M." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1734m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: BOLT SHEARED ON RIG FLOOR STAND-LIFTER; REPLACED BOLT." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 500m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: CONTINUED POOH WITH FMT TOOLSTRING FROM 1734 - 500 M." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: COMPLETED POOH WITH FMT TOOLSTRING ON DRILLPIPE. LD FMT TOOLSTRING." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 11m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: MU SIDEWALL CORE TOOLSTRING & PIPE CONVEYED LOGGING TOOLS." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3183m. The activity was categorized as 'formation evaluation -- log' and lasted for 8.5 hours. Operational details: RIH WITH SIDEWALL CORE TOOLSTRING TO 3183 M." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3183m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS-UP TO BALANCE MUD - 1000 LPM Ø 169 BAR. MAXIMUM GAS READING DURING CIRCULATION = 55% - SOURCE = WELLHEAD." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3189m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: MU STABILIZER + SIDE ENTRY SUB INTO DRILLPIPE STRING. ATLAS RIH WITH WET CONNECTOR ON ELECTRIC LINE - WHILE PUMPING 400 LPM Ø 41 BAR. WHILE PUMPING 1330 LPM Ø 320 BAR IN SUCCESSFUL ATTEMPT TO LATCH WET CONNECTOR, RUBBER PACKING IN SIDE ENTRY SUB WASHED-OUT OR POPPED-OUT. INSTALLED NEW RUBBER PACKING INTO SIDE ENTRY SUB." "On 1998-01-17, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3219m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: RIH WITH SIDEWALL CORE TOOLSTRING ON DRILLPIPE FROM 3189 - 3219 M." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4230m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.0 hours. Operational details: CONTINUED TO RIH WITH SIDEWALL CORING TOOLSTRING FROM 3219 - 4230 M." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3920m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: RAN CORRELATION LOG. START POOH WITH SIDEWALL CORING TOOLSTRING/DRILLPIPE - TAKING 2 SIDEWALL CORES PER STATION WHILE POOH. 30 OUT OF 50 SIDEWALL CORES TAKEN." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3770m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: CONTINUED TO POOH WITH SIDEWALL CORING TOOLSTRING/DRILLPIPE FROM 3920-3770 M. TOOK SIDEWALL CORES WHILE POOH." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3189m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: COMPLETED TAKING SIDEWALL CORES. CONTINUED TO POOH WITH SIDEWALL CORING TOOLSTRING/DRILLPIPE TO 3189 M." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3189m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: ATLAS PULLED WET CONNECTOR LOOSE WITH NO PROBLEMS; 7000 LBS.-3,2 MT- OF PULL NEEDED. ATLAS POOH WITH ELECTRIC LINE. RD SIDE ENTRY SUB & LD STABILIZER." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3189m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: RD ATLAS WIRELINE SHEAVES FROM DERRICK." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 7.5 hours. Operational details: COMPLETED POOH WITH SIDEWALL CORING TOOLSTRING/DRILLPIPE. LD SIDEWALL CORING TOOLSTRING." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 241m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.0 hours. Operational details: RU 2 7/8' TUBING HANDLING EQUIPMENT.PU CEMENT MULESHOE+24 JTS. 2 7/8' TUBING FOR P&A CEMENT PLUGS." "On 1998-01-18, at Well NO 15/9-19 B, a drilling event occurred at a depth of 950m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: CONTINUED TIH WITH CEMENT STINGER FROM 241 - 950 M." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2840m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.0 hours. Operational details: CONTINUED TO TIH WITH CEMENT STINGER FROM 950 - 2840 M. MU CEMENTING JOINT/5' DP BEFORE CONTINUING TO TIH TO SPOT FIRST PLUG." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2840m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: FINISHED MU CEMENTING ASSEMBLY FOR SPOTTING P&A PLUGS. SERVICED TOP DRIVE & IRON ROUGHNECK + PERFORMED ELECTRICAL TESTS ON DRAWWORKS WHILE MONITORING WEATHER. (2 7/8' MULESHOE 10 STANDS INSIDE 7' SHOE.)" "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4246m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: CONTINUED TO TIH FROM 2835 TO 4246 M." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4246m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED - 870 LPM Ø 192 BAR." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3584m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: WEATHER DRASTICALLY INCREASED;DECISION MADE TO POOH & HANG-OFF.PUMPED 2 SLUGS DUE TO EXCESSIVE U-TUBING OF MUD;UNSUCCESSFUL IN STOPPING U-TUBING OF MUD UP STRING. POOH FROM 4246 TO 3584 M; MUD CONSTANTLY U- TUBING UP STRING." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: DUE TO RIG HEAVES, STOPPED POOH & MU FMC HANG-OFF-TOOL (WITH IBOP BELOW TOOL) INTO DRILLPIPE STRING. RIH TO WELLHEAD & LANDED STRING IN WELLHEAD-2 7/8' TUBING Ø 3694M-& RELEASED HANG-OFF-TOOL'S RUNNING TOOL CLOSED LOWER PIPE RAMS." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: POOH WITH DRILLPIPE + HANG-OFF-TOOL'S RUNNING TOOL. DISPLACED OIL BASE MUD FROM RISER USING SEAWATER - DISPLACED VIA CHOKE LINE. CLOSED BLIND/SHEAR RAMS & BLOCKED ALL STACK FUNCTIONS. UNLATCHED Ø 1755 HRS. DUE TO 10 M HEAVE." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: DE-BALLASTED RIG 3 M TO 18,2M-SURVIVAL DRAFT." "On 1998-01-19, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: WAITED ON WEATHER." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WAITED ON WEATHER." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: CONTINUED WAITING-ON-WEATHER." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: SLIPPED & CUT DRILLINE WHILE BALLASTED-DOWN RIG FROM 18,2 M TO 21,3 M DRAFT." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: RU RISER HANDLING EQUIPMENT." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: PULLED DIVERTER & LD SAME." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: RU RISER LIFTING SUB & MU 1 STAND OF 5' DRILLPIPE. COLLAPSED INNER BARREL OF SLIP JOINT & LOCKED SAME." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: PREPARED T0 LAUNCH ROV." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: LAUNCHED ROV. MOVED RIG PORT AFT IN ORDER TO LAND LMRP ONTO BOPS." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: LANDED LMRP ONTO BOPS. RECONNECTED LMRP & PERFORMED 22,7 MT OVERPULL TEST. TESTED CHOKE & KILL LINES TO 35 BAR FOR 5 MIN.;345 BAR FOR 10 MIN.-WHILE STROKING OUT SLIP JOINT'S INNER BARREL. RU TO RUN DIVERTER." "On 1998-01-20, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: OPENED FAILSAFE VALVES & CHECKED FOR PRESSURE BELOW BLIND/SHEAR RAMS- NO PRESSURE. CIRCULATED MUD DOWN KILL LINE & UP CHOKE LINE. LANDED DIVERTER. OPENED LPR & CHECKED FOR PRESSURE-NO PRESSURE. CIRCULATED MUD DOWN KILL LINE & UP CHOKE LINE-TOOK 0,8 M3 MUD TO FILL HOLE BEFORE RETURNS TO TRIP TANK. CLOSED LPR." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: COMPLETED NU DIVERTER. RD RISER SPIDER/RISER HANDLING EQUIPMENT." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3694m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: RIH WITH 5' DRILLPIPE TO RETRIEVE HANG-OFF-TOOL. OPENED BLIND/SHEAR RAMS & COMPLETED RIH TO WELLHEAD.MU DRILLPIPE INTO HANG-OFF-TOOL." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3581m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: DISPLACED RISER WITH OIL BASE MUD BY CIRCULATING DOWN CHOKE & KILL LINES. OPENED LPR & PULLED HANG-OFF-TOOL OUT OF WELLHEAD - 54 MT OF OVERPULL REQUIRED / 186 MT WEIGHT INDICATOR READING. POOH WITH HANG-OFF-TOOL TO SURFACE & BROKE-OUT SAME FROM DRILLPIPE; MUD U-TUBING UP DRILLPIPE. SECURE DRILLPIPE WITH IBOP & STOOD BACK HANG-OFF-TOOL." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3581m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: CIRCULATED DOWN DRILLPIPE TO BALANCE MUD - 1000 LPM Ø 210-230 BAR. MUD WEIGHT OUT BEFORE BOTTOMS-UP = 1,45 SG. MAXIMUM GAS READING = 25%. FINE SOLIDS ON BOTTOMS-UP BLINDED SCREENS; HAD TO CHANGE SCREENS. AFTER BOTTOMS-UP 1000 LPM = 186 BAR. NO MUD LOSSES DOWNHOLE WHILE CIRCULATING. HOLE 'STICKY' Ø3558M & 3577M-STALLING TOP DRIVE." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3581m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: CONTINUED TO CIRCULATE IN ORDER TO BALANCE MUD. REMOVED GREY IBOP FROM STRING." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3558m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: WHILE POOH FROM 3694-3558 M, PIPE STUCK Ø 3558 M. COULD ROTATE BUT UNABLE TO PULL ABOVE 3558M. WORKED STRING FREE WITH MAXIMUM OF 50 MT OVERPULL." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3469m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: CONTINUED TO POOH TO 3469 M - TO GET ABOVE TIGHT SPOT.PU HANG-OFF-TOOL & INSTALLED COURSE THREADED RELEASE SUB BACK INTO TOOL'S STAND. STOOD HANG-OFF-TOOL BACK IN DERRICK." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3498m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: RIH TO 3498 M. MUD U-TUBING FROM DRILLPIPE. CIRCULATED TO BALANCE MUD." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: RIH FROM 3498 - 4250 M - TD." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED 1,5 TIMES BOTTOMS-UP TO BALANCE MUD PRIOR TO SETTING BALANCED CEMENT PLUG; 1000 LPM Ø 203 BAR." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: MU CEMENTING STAND INTO STRING & TESTED CEMENT LINE TO 345 BAR FOR 5 MINUTES." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4250m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: SPOTTED CEMENT PLUG NUMBER 1 FROM 4250 - 4025 M. PUMPED 2 M3 1,69SG SPACER, 5,1 M3 1,90 SG CEMENT SLURRY, 0,35 M3 1,69 SG SPACER & DISPLACED WITH 21,3 M3 1,40 SG MUD." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4025m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH TO 4025 M." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4025m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.5 hours. Operational details: CIRCULATED ONE HOLE VOLUME; 945 LPM Ø 189 BAR." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4025m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: MU CEMENTING STAND INTO DRILLPIPE & TESTED CEMENT LINE TO 345 BAR FOR 5 MINUTES." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 4025m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: SPOTTED CEMENT PLUG NUMBER 2 FROM 4025 - 3800 M. PUMPED 2,0 M3 1,69 SG SPACER, 5,1 M3 1,90 SG CEMENT SLURRY, 0,35 M3 1,69 SG SPACER & DISPLACED WITH 18,9 M3 1,40 SG MUD. NOTE:PIPE STUCK MOMENTARILY WHILE CEMENTING;FREED WITH 73 MT OVERPULL." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3660m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH FROM 4025 - 3660 M. HOLE TOOK 1,07 M3 OF ADDITIONAL FILL ON TRIP OUT OF HOLE; TOOK 27 MT OVERPULL TO PULL PAST TIGHT SPOT Ø 3878 M." "On 1998-01-21, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3660m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.5 hours. Operational details: STARTED CIRCULATING BOTTOMS-UP Ø 3660M; 500 LPM Ø 65 BAR. MAXIMUM GAS READING = 7,2%; HAD TO ROTATE STRING CONSTANTLY BECAUSE OF 'STICKING PROBLEMS'." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3660m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.0 hours. Operational details: BOOSTED RISER WITH ADDITIONAL MUD PUMP ONCE BOTTOMS-UP WAS ABOVE WELLHEAD & COMPLETED CIRCULATING BOTTOMS-UP. NO SPACER OR CEMENT RETURNS. SPOTTED 6 M3 OF 'TRASH LCM' MUD IN HOLE." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3350m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH FROM 3660 - 3350 M." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3350m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: PUMPED 4 M3 HI-VIS PILL & DISPLACED TO END OF DRILLPIPE;650LPMØ107BAR." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3250m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH FROM 3350 - 3250 M WHILE PUMPING/SPOTTING HI-VIS PILL FROM 3350 - 3250 M." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3250m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS-UP; 800 LPM Ø 131 BAR. BOOSTED RISER WITH ADDITIONAL MUD PUMP ONCE BOTTOMS-UP WAS ABOVE WELLHEAD TO REDUCE CIRCULATING TIME." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3250m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: MU CEMENTING STAND INTO DRILLPIPE & TESTED LINE TO 345 BAR FOR 5 MINUTES." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3250m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: SPOTTED CEMENT PLUG NUMBER 3 FROM 3250 - 3100 M. PUMPED 1,8 M3 1,69 SG SPACER, 4 M3 1,95 SG CEMENT SLURRY, 0,61 SG SPACER & DISPLACED WITH 12,57 M3 1,40 SG OIL BASE MUD." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2940m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH FROM 3250 - 2940 M. HOLE TOOK 1 M3 OF ADDITIONAL FILL ON TRIP OUT OF HOLE." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2940m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 4.0 hours. Operational details: CIRCULATED BOTTOMS-UP ; 500 LPM Ø 62 BAR. NOTE: BOOSTED RISER ONCE BOTTOMS-UP ABOVE WELLHEAD TO REDUCE CIRCULATING TIME." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1812m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.5 hours. Operational details: POOH FROM 2940-1812 M; LD 39 JTS. 5' DRILLPIPE + 78 JTS. 3 1/2' DRILLPIPE WHILE POOH." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 241m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.5 hours. Operational details: CONTINUED TO POOH FROM 1812 - 241 M WITH 3 1/2' DRILLPIPE." "On 1998-01-22, at Well NO 15/9-19 B, a drilling event occurred at a depth of 158m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: LD 9 JTS. 2 7/8' TUBING - CEMENT STINGER." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: COMPLETED LD 15 JTS. 2 7/8' TUBING + MULESHOE. NOTE:STARTED LOSING MUD Ø0000 HRS.STOPPED OPERATIONS FOR APPROXIMATELY 1/2 HOUR & CHECKED TRIP TANK + OTHER SURFACE EQUIPMENT/SLIP JOINT FOR LEAKS. BETWEEN 0000 - 0230 HRS. TRIP TANK DROPPED 6,4 M3 MORE THAN CALCULATED HOLE FILL FOR TUBULARS." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: WHILE CLEANING RIG FLOOR & PREPARING TO MU BHA, VISUALLY OBSERVED ANNULUS LEVEL DROP IN RISER. CLOSED BLIND/SHEAR RAMS; RATE OF MUD LOSS DID NOT DECREASE; 1,3 M3 LOST IN 30 MINUTES.OPENED BLIND/SHEAR RAMS - MUD NEEDED TO FILL HOLE BELOW RAMS WAS NEGLIGIBLE." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 293m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: MU 5 7/8' BIT & BHA FOR TESTING OF PLUG NUMBER 3. RAN 4 STANDS 3 1/2' DRILLPIPE TO 293 M - PLACING DRILLPIPE ACROSS UPPER ANNULAR PREVENTER. RATE OF LOSS TO HOLE VIA TRIP TANK REMAINED CONSTANT - APPROXIMATELY 2 M3/HOUR." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 293m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: WITH BIT Ø 293 M, CLOSED UPPER ANNULAR ON 3 1/2' DP. 0,6 M3 MUD LOST DOWN ANNULUS IN 20 MINUTES - VERIFIED THAT MUD LOSS WAS DUE TO LEAK IN RISER SYSTEM - ABOVE UPPER ANNULAR PREVENTER. OPENED UPPER ANNULAR." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 640m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: CONTINUED TO RIH FROM 293 - 640 M." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 640m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: REPAIRED BURST HYDRAULIC HOSE ON UPPER RACKING ARM. NOTE: MOVED RIG 3 M Ø APPROXIMATELY 0830 HRS. & SLOWED LEAK FROM RISER TO 0,3 M3 / HOUR." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 640m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: PRESSURE TESTED CEMENT PLUG NUMBER 3 TO 70 BAR FOR 15 MINUTES BEFORE DISPLACING RISER TO SEAWATER." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 640m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: DISPLACED OIL BASE MUD WITH SEAWATER - FROM 640 M TO SURFACE - IN ORDER TO PREVENT ADDITIONAL LEAKAGE OF OIL BASE MUD FROM RISER." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.0 hours. Operational details: CONTINUED RIH WITH 5 7/8' BIT FROM 640 - 3146 M." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: TAGGED TOP OF CEMENT PLUG NUMBER 3 Ø 3146 M. WEIGHT TESTED PLUG BY SLACKING-OFF 10 MT DOWN." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.5 hours. Operational details: DISPLACED OIL BASE MUD WITH 1,40 SG WATER BASE MUD." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: NEEDED 20 M3 ADDITIONAL WATER BASE MUD TO FINISH DISPLACEMENT; BUILT 1,40 SG WATER BASE MUD." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: COMPLETED DISPLACING HOLE TO 1,40 SG WATER BASE MUD." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: CLOSED UPPER ANNULAR & TESTED CEMENT PLUG NUMBER 3 TO 120 BAR FOR 15 MINUTES. UNABLE TO CONTINUE BUILDING WATER BASE MUD WHILE PUMPING OIL BASE MUD ONBOARD SUPPLY BOAT." "On 1998-01-23, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: COMPLETED PUMPING TRASH OIL BASE MUD TO BOAT. CONTINUED TO BUILD 1,40 SG WATER BASE MUD FOR SLUGGING DRILLPIPE & FOR FILLING HOLE ON TRIP OUT OF HOLE." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: COMPLETED BUILDING 1,40 SG WATER BASE MUD FOR TRIP OUT OF HOLE." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 3146m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED 1 DP VOLUME TO SHEAR THICK MUD WHILE BUILDING SLUG. BUILD SLUG FOR TRIP OUT OF HOLE." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 2639m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.5 hours. Operational details: POOH - LD 5' DRILLPIPE ON TRIP OUT OF HOLE. AT REPORT TIME - 52 JTS. LD - BIT DEPTH = 2639 M. NOTE: LOSING APPROXIMATELY 1,5 M3/HR. VIA RISER LEAK." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 178m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.0 hours. Operational details: CONTINUED TO POOH FROM 2639-178 M/TOP OF BHA. LD TOTAL OF 84 JTS. 5' DRILLPIPE ON TRIP OUT OF HOLE. NOTE:Ø 0700 HRS. DISPLACED RISER TO SEAWATER VIA CHOKE LINE BECAUSE RISER LEAK STARTED AGAIN. LOST 3,3 M3 WATER BASE MUD VIA RISER BEFORE DISPLACING MUD FROM RISER." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: LD 9 JTS. 3 1/2' HWDP, 1 - JAR, + 9-4 3/4' DC / BHA / WHILE POOH." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: RIH & RETRIEVED 9 5/8' WEAR BUSHING FROM WELLHEAD." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- cut' and lasted for 7.0 hours. Operational details: MU 9 5/8' CASING CUTTING ASSEMBLY & RIH; LANDED MARINE SWIVEL INTO WELLHEAD - SPACED-OUT CUTTERS Ø 1485 M. DISPLACED RISER BACK TO 1,40 SG WATER BASE MUD Ø 2030 HRS. - VIA CHOKE LINE." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: CUT 9 5/8' CASING Ø 1485 M - WITH UPPER ANNULAR CLOSED. FREE ROTATING TORQUE BEFORE = 7860 NM. WHILE CUTTING TORQUE = 10800 NM PUMP PRESSURE = 76 BAR Ø 540 LPM. AFTER CUT TORQUE RETURNED TO 7860 NM PUMP PRESSURE = 38 BAR Ø 540 LPM. NOTE: ROTARY SPEED = 140 RPM WHILE CUTTING." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: SWEPT GAS FROM BOPS VIA SEAWATER & MUD. CLOSED LOWER ANNULAR & OPENED UPPER ANNULAR & ALLOWED TRAPPED GAS TO MIGRATE UP RISER. THEN OPENED LOWER ANNULAR & ALLOWED GAS TO AGAIN MIGRATE UP RISER. NOTE: VISUALLY OBSERVED GAS 'BREAKING-OUT'. ALSO OBSERVED MUD LEVEL DROPPING IN RISER ANNULUS; RISER LEAKING AGAIN." "On 1998-01-24, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS-UP FROM 1485 M. UNABLE TO CIRCULATE FASTER THAN 800 LPM BECAUSE LOSING SUCTION DUE TO HIGH VISCOSITY OF WATER BASE MUD." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1485m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: COMPLETED CIRCULATING BOTTOMS-UP. MAXIMUM GAS READING = 4%. FLOW CHECKED, PUMPED SLUG & DISPLACED RISER BACK TO SEAWATER." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 4.0 hours. Operational details: POOH WITH CASING CUTTING ASSEMBLY- STOOD BACK TUBULARS FOR FUTURE USE. NOTE:LD 2 JTS. 5' HWDP TO ACCOMODATE STANDING-BACK OF CUTTING ASSEMBLY" "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 30m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH WITH FMC SPRING-LOADED TOOL TO RETRIEVE SEAL ASSEMBLY" "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH TO WELLHEAD WITH FMC SPRING-LOADED TOOL. MU INTO SEAL ASSEMBLY. CLOSED UPPER ANNULAR & PU 2,5 MT TO PULL SEAL ASSEMBLY FREE." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: GAS MIGRATED UP RISER - PAST THE CLOSED ANNULAR. SWEPT GAS FROM BOPS USING SEAWATER. CLOSED LOWER ANNULAR & OPENED UPPER ANNULAR; ALLOWED GAS TO MIGRATE UP RISER. OPENED LOWER ANNULAR & ALLOWED GAS TO MIGRATE" "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH - DIDN'T RECOVER SEAL ASSEMBLY." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: RIH AGAIN WITH SPRING-LOADED TOOL. MU INTO SEAL ASSEMBLY & PU 4 MT TO PULL SEAL ASSEMBLY FREE. ADDITIONAL GAS MIGRATED UP RISER.SHUT-IN WELL & BLED GAS OFF. SWEPT GAS FROM BOPS USING SEAWATER. OPENED WELL & POOH WITH SEAL ASSEMBLY. LD SEAL ASSEMBLY; STAND BACK TOOL." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 182m. The activity was categorized as 'plug abandon -- cut' and lasted for 3.5 hours. Operational details: MU 9 5/8' CASING SPEAR WITH PACK-OFF. RIH - PU 14 JTS. 5' 25,6# U170 DRILLPIPE. ENGAGED 9 5/8' CASING WITH SPEAR Ø 182 M - 1 M BELOW 10 3/4' X 9 5/8' X/OVER. NOTE: 9 5/8' CASING CUT Ø DEPTH OF 1485 M." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 162m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: PULLED 9 5/8' X 10 3/4' STRING FREE WITH NO ADDITIONAL OVERPULL. HAD TO MANUEVER STRING TO PULL CASING THROUGH THE ANNULARS. PU CASING HANGER 20 M ABOVE WELLHEAD. NOTE: CASING CUT NOW Ø 1465 M; SPEAR Ø 162 M." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 162m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: CLOSED UPPER ANNULAR & ESTABLISHED INJECTION INTO FORMATION.BULLHEADED DOWN 10 3/4'-9 5/8' X 13 3/8' ANNULUS VIA UPPER CHOKE LINE Ø 935 LPM: 31,3 M3 'TRASH' OIL BASE MUD & 50 M3 1,40 SG WATER BASE MUD. PRESSURE DECREASED FROM 103 BAR TO 55 BAR WHEN WATER BASE MUD REACHED 13 3/8' SHOE/FORMATION." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 162m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: MONITORED SHUT-IN PRESSURE - 45 BAR. BLED-OFF PRESSURE, IN STAGES, TO 0 BAR; BLED BACK A TOTAL OF 3 M3." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1465m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: OPENED UPPER ANNULAR & STARTED CIRCULATING BOTTOMS-UP; SPEAR Ø 162 M & CASING CUT Ø 1465 M. STOPPED CIRCULATING WATER BASE MUD Ø 1920 HRS. BECAUSE LOST 3,5 M3 MUD FROM LEAK IN SLIP JOINT. NOTE: MUD WEIGHT IN = 1,38 SG; MUD WEIGHT OUT = 1,33 SG." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1465m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: SLIP JOINT LEAK CAUSED LOSS OF PUMP SUCTION - TRANFERRED MUD TO A.PIT TO ALLOW REGAINING OF PUMP SUCTION. NOTE: RIG DOWNTIME." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1465m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: UNABLE TO WEIGHT-UP MUD TO 1,40 SG BECAUSE COULDN'T OBTAIN BARITE INTO PUMP ROOM'S SURGE CAN. NOTE: RIG DOWNTIME." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1465m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: INVESTIGATE BARITE SITUATION - CHECK BARITE TANKS ." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1465m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: DISPLACED WATER BASE MUD IN RISER WITH SEAWATER - DUE TO LEAKING RISER. CLOSED UPPER ANNULAR & MONITORED HOLE VIA CHOKE LINE - LEAK IN RISER DOESN'T ALLOW 'CORRECT' MONITORING OF HOLE. HOLE STATIC; OPENED UPPER ANNULAR. NOTE: RIG DOWNTIME." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1427m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH WITH SPEAR + CASING STRING; SPEAR PULLED FROM 162 - 124 M - CASING PULLED FROM 1465 - 1427 M." "On 1998-01-25, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1427m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: AIR HOSE TO PNEUMATIC DRILLPIPE ELEVATORS BURST. REMOVED AIR HOSE & RU MANUAL DRILLPIPE ELEVATORS." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1378m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: CONTINUED TO POOH WITH DRILLPIPE/SPEAR + CASING STRING - UNTIL 10 3/4' CASING HANGER Ø SURFACE. WITH SPEAR 75M BELOW ROTARY, RELEASED SPEAR." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1378m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: RU FALSE ROTARY. COMPLETED POOH WITH SPEAR & PACK-OFF ASSEMBLY. NOTE: CASING CUT Ø 1378 M." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1200m. The activity was categorized as 'plug abandon -- cut' and lasted for 3.0 hours. Operational details: POOH WITH 10 3/4' X 9 5/8' CASING STRING. LD CASING HANGER, 5 JTS. 10 3/4', X/OVER & 6 JTS. 9 5/8' AS OF 0600HRS" "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 7.0 hours. Operational details: COMPLETED LD 9 5/8' CASING: TOTAL OF 103 JTS. 9 5/8' CASING RECOVERED." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: RD CASING TOOLS." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: REPLACED AIR HOSE FOR DRILLPIPE ELEVATORS." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1640m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.5 hours. Operational details: MU 3 1/2' CEMENTING MULE SHOE AND RIH WITH 3 1/2' AND 5' DRILLPIPE TO 1640 M." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1640m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED MUD WEIGHTED UP TO 1.40 SG. MAX GAS READING = 36.6 O/O." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1640m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: SPOTTED HI-VIS PILL FROM 1640 - 1540 M." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1540m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH TO 1540 M. RU TO CEMENT." "On 1998-01-26, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1540m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: STARTED SPOTTING CEMENT PLUG NUMBER 4 FROM 1540 - 1385 M. PUMPED 3M3 DRILL WATER SPACER." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1540m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: COMPLETED PUMPING 9.8 M3 1,9 SG CEMENT SLURRY, 0.3 M3 DRILL WATER + 4 M3 1,40 SG WATER BASE MUD." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1350m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH FROM 1540 - 1350 M." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1350m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS-UP/CEMENT IN RETURNS AT BOTTOM-UP. DISPLACED RISER TO SEAWATER. DUMPED CONTAMINATED MUD AT SHAKERS." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 620m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: POOH - LD 3 1/2' DP ON TRIP OUT. (52 JTS LD AS OF REPORT TIME)." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: COMPLETED POOH WITH 3 1/2' MULESHOE. LD A TOTAL OF 111 JTS. 3 1/2' DP ON TRIP OUT." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1350m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.0 hours. Operational details: MU 12 1/4' BIT AND 13 3/8' SCRAPER BHA AND RIH. SCRAPED AREA AROUND 1350 M ON TRIP-IN-HOLE." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1371m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: TAGGED CEMENT PLUG NUMBER 4 AT 1371 M - 14 M HIGH. WEIGHT TESTED PLUG WITH 10 MT; PRESSURE TESTED TO 102 BAR FOR 10 MINUTES." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1640m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.0 hours. Operational details: POOH WITH 12 1/4' BIT AND SCRAPER BHA. LD 96 JTS. 5' DRILLPIPE ON TRIP-OUT-OF-HOLE." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 1209m. The activity was categorized as 'plug abandon -- cut' and lasted for 4.0 hours. Operational details: RU ATLAS ELECTRIC LINE. RIH WITH 13 3/8' BRIDGE PLUG ON ELECTRIC LINE; STARTED DRAGGING AT 1209 M - ON 3RD ATTEMPT MADE PROGRESS TO 1214 M. SET BRIDGE PLUG AT 1209 M (TOP OF PLUG). POOH AND RD ATLAS." "On 1998-01-27, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: MU 13 3/8' CASING CUTTING ASSEMBLY." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 211m. The activity was categorized as 'plug abandon -- cut' and lasted for 3.0 hours. Operational details: COMPLETED MU ASSEMBLY AND RIH - LANDED MARINE SWIVEL INTO WELLHEAD - SPACED-OUT CUTTERS ON 211 M. CLOSED UPPER ANNULAR." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 211m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: CUT 13 3/8' CASING AT 211 M WITH UPPER ANNULAR CLOSED. FREE ROTATING TORQUE BEFORE = 2700 NM: WHILE CUTTING = 5400-13500 NM; AFTER CUTTING = 2700 NM. WHILE CUTTING PUMP PRESSURE = 76 BAR AT 1220 LPM; AFTER CUTTING PUMP PRESSURE = 31 BAR. ROTARY SPEED WHILE CUTTING = 120 RPM." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 211m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: SWEPT GAS FROM BOPS USING SEAWATER AND MUD. ALLOWED GAS TO MIGRATE UP RISER. CLOSED LOWER ANNULAR AND OPENED UPPER ANNULAR. ALLOWED GAS TO MIGRATE. OPENED LOWER ANNULAR - GAS MIGRATED RAPIDLY. CLOSED DIVERTER PACKER. WAITED 10 MINUTES AND OPENED PACKER. GAS STILL MIGRATING UP RISER." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 211m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS-UP FROM 211 M - DEPTH OF 13 3/8' CUT. MAXIMUM GAS READING = 63 O/O." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 211m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: DISPLACED RISER FROM MUD TO SEAWATER." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH WITH 13 3/8' CASING CUTTER ASSEMBLY. STOOD BACK IN DERRICK." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: RIH WITH FMC SPRING LOADED TOOL TO WELLHEAD, MU TOOL INTO SEAL ASSEMBLY. CLOSED ANNULAR AND PULLED SEAL ASSEMBLY FREE, SWEPT BOPS FOR GAS. NO GAS PRESENT. OPENED ANNULAR AND POOH WITH SEAL ASSEMBLY." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 108m. The activity was categorized as 'plug abandon -- cut' and lasted for 5.0 hours. Operational details: MU 13 3/8' SPEAR/PACK-OFF ASSEMBLY. ENGAGED 13 3/8' CASING BELOW WELL- HEAD. UNABLE TO PULL 13 3/8' CASING FREE WITH 154 MT OVERPULL. ESTABLISHED INJECTION - 680 LPM AT 16 BAR. RELEASED SPEAR AND POOH." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: RD WEATHERFORD'S POWERMASTER FRAME AND TOOLS. LD BAKER'S CASING CUTTING AND PULLING TOOLS FROM DERRICK." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 462m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: RIH WITH 3 1/2' MULESHOE AND DRILLPIPE TO 462 M. POOH TO 350 M - LD 11 JTS - 3 1/2' DRILLPIPE." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: SPOTTED 1,40 SG HI-VIS PILL FROM 350 - 250 M." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 125m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH TO 125 M. LD 24 JTS - 3 1/2' DRILLPIPE." "On 1998-01-28, at Well NO 15/9-19 B, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: RIH WITH 5' DRILLPIPE TO 250 M." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: MU CEMENTING STAND. RU HOSE." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: SPOTTED CEMENT PLUG NUMBER 5 IN 13 3/8' CASING FROM 250 - 125 M. PUMPED 3 M3 DRILLWATER SPACER, 9,8 M3 1,92 SG CEMENT SLURRY, 5 M3 DRILLWATER SPACER." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 124m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: POOH TO 124 M. CLOSED UPPER PIPE RAM. SQUEEZED 1,95 M3 MUD DOWN CHOKE LINE. 10 BAR AT ,5 M3 PER MINUTE. FINAL SHUT-IN PRESSURE = 10 BAR. BLED OFF ,9 M3. OPENED RAM. CIRCULATED CEMENT BACK TO SURFACE 3,4 M3 EARLY. SPLIT PUMPS AND FLUSHED CHOKE LINE WHILE CIRCULATING DOWN STRING." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 150m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: WASHED DOWN TO 150 M. 1 PUMP ON ON RISER, 1 PUMP ON STRING. CIRCULATED UNTIL NO CEMENT IN RETURNS. (TOP OF CEMENT = 150 M)." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH TO BOPS AND JET CLEAN. POOH. LD 3 1/2' DRILLPIPE." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 8.0 hours. Operational details: CONTINUED LD 3 1/2'DP. LD DOWN FROM DERRICK; 5' DP, 5' HWDP, 6 1/2' DC AND BROKE DOWN EMERGENCY HANG OFF TOOL." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: SLIP AND CUT DRILLING LINE." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 96m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: RU TO PULL LMRP. HELD PRE-JOB SAFETY MEETING WITH INVOLVED PERSONNEL" "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 96m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: PULLED AND LAID DOWN DIVERTER ASSY." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 96m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: PICKED UP 2 RISERS AND MADE UP TO SLIP JT." "On 1998-01-29, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: PERFORMED 50 TON OVERPULL TEST AND UNLATCHED LMRP AT 2135 HRS. REMOVED KILL/ CHOKE/ BOOSTER LINES AND POD LINE SADDLES." "On 1998-01-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CONTINUED RIGGING DOWN FROM SLIP JT. STORED RISER SUPPORT RING." "On 1998-01-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: MOVED RIG 30M OFF LOCATION IN 020 DEGR DIRECTION." "On 1998-01-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: PULLED LMPR TO SPLASH SONE." "On 1998-01-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CONTINUED PULLING LMRP TO MOONPOOL." "On 1998-01-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: SECURED LMRP AND DISMANTLED POD FEMALE RECEPTICALS IN ORDER TO LAND LMRP ONTO SKID BEAMS. SET DOWN LMPR OK." "On 1998-01-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: REMOVED BULLSEYE AND POSITION BEACON AND DISCONNECTED RISER JOINT. INSPECTED FLEX JOINT AND FOUND 3 KEY SEATS." "On 1998-01-30, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 12.0 hours. Operational details: MOVED LMRP TO FWD SIDE IN MOONPOOL. DISCONECTED KILL AND CHOKE LINE COFLEX HOSES AND FLEX JOINT." "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: MADE UP NEW FLEX JOINT AND INSTALL ON LMRP. TRANSPORTED LMRP ONTO LANDING BEAMS AND MADE UP TO RISER JT." "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: MOUNTED POD FEMALE RECEPTICALS AND INSTALLED 1 POD AND 2 GUIDELINES" "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 98m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: RAN IN WITH LMRP TO 9 M ABOVE GUIDE POSTS." "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 98m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: POSITIONED RIG FROM STB SIDE TO WELL CENTER." "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 110m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: PREPARED TO LAND LMRP. LANDED AT 1830 HRS AND PERFORMED OVER PULL TEST AFTER CONFIRMED LATCH WITH 25 T." "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: UNLATCHED BOP AND PULLED 2M ABOVE WELLHEAD. TOP OF BOP FRAME BUMPER INTERFERED WITH TEMPLATE STRUCTURE AT AFT SIDE. PULLED RIG 5M FORWARD AND PULLED BOP 8M ABOVE GUIDE POSTS." "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: MOVED RIG 30M OFF LOCATION IN 020 DEGR DIRECTION." "On 1998-01-31, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: PULLED BOP AND LANDED ON SKID BEAMS. DISCONNECTED RISER AND REMOVED GUIDELINES." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: STORED AND SECURED LMRP AND BOP. LAYED DOWN 2 RISER JOINTS." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIGGED DOWN RISER HANDLING EQUIPMENT AND MOVED RIG TO WELL CENTER." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 110m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH AND SET CORROSION CAP. SHEARED PINS WITH 9T OVERPULL. RELEASED AND RETRIEVED GUIDELINES." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH WITH WIRE SLING ON DP AND ENGAGED PROTECTION HATCH. MOVED HATCH TO WELL CENTER." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: INSTALLED PROTECTION HATCH AND DISCONNECTED LIFTING FRAME FROM HATCH. PULLED LIFTING FRAME TO MOONPOOL." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: REMOVED LIFTING FRAME FROM CELLAR DECK." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH WITH WIRE SLING ON DP AND RETRIEVED HANDRAIL FROM TEMP PLATE ROOF." "On 1998-02-01, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 12.0 hours. Operational details: DE-BALLASTED RIG TO 7,6M DRAFT. STARTED ANCHOR HANDLING AT 1955 HRS; ANCHORS IN BOLSTER AT; NO 11/ 2143 HRS, NO 5/ 2159 HRS." "On 1998-02-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 5.0 hours. Operational details: CONTINUED ANCHOR HANDLING; ANCHOR NO 12 IN BOLSTER 0002 HRS PENNANT NO 1 SECURED; 0051 HRS, PENNANT NO 6 SECURED; 0218 HRS PENNANT NO 3 SECURED; 0258 HRS. ANCHOR NO 9 IN BOLSTER 0441 HRS. ANCHOR NO 1,3 AND 6 REMOVED FROM CHAINS FOR MOORING PURPOSE." "On 1998-02-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WAITING ON WEATHER DUE TO HIGH WIND; 22 TO 25 M/S WITH WAVE HEIGHT 4M." "On 1998-02-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: W.O.W. DUE TO HIGH WIND: 23-24 M/S 4-5 M WAVE HEIGHT. PACIFIC BUCCANEER IN TOWING BRIDLE." "On 1998-02-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: DEBALLASTED RIG DOWN TO SURVIVAL DRAFT (18,2M)." "On 1998-02-02, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 11.0 hours. Operational details: WAIT ON WEATHER DUE TO HIGH WINDS AND WAVE HEIGHT; MAX 25 M/S WITH 6 M WAVE HEIGHT." "On 1998-02-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: CONTINUED WAIT ON WEATHER; 0100 HRS: 14 M/S DIRECTION 340, 4-6 M WAVE 0200 HRS; 15 M/S DIRECTION 340, 4-6 M WAVE 0300 HRS; 16 M/S DIRECTION 340, 4-6 M WAVE" "On 1998-02-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: STARTED DEBALLAST RIG TO COMMENCE ANCHOR HANDLING AT 0330 HRS. WEATHER CONDITIONS: 0400 HRS: 15 M/S DIRECTION 340, 4-6 M WAVE 0500 HRS; 10 M/S DIRECTION 340, 4-6 M WAVE 0600 HRS; 8 M/S DIRECTION 320, 4-6 M WAVE" "On 1998-02-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: CONTINUED DEBALLAST RIG TO TRANSIT DRAFT." "On 1998-02-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 6.5 hours. Operational details: COMMENCED ANCHOR HANDLING: ANCHOR # 10 BOLSTRED 11,59 HRS N CRUSADER ANCHOR # 2 BOLSTRED 13,52 HRS STRIL POWER ANCHOR # 4 BOLSTRED 13,57 HRS N CRUSADER ANCHOR # 8 BOLSTRED 15,30 HRS N CRUSADER LOST ANCHOR # 7 SEABED 15,50 HRS STRIL POWER" "On 1998-02-03, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 8.0 hours. Operational details: RIG ON TOW TO ØLEN. PACIFIC BUCCANEER IN TOWING BRIDLE. POSITION FOR LOST ANCHOR: LAT: 58 DEG 25 MIN 28,328 SEC N LONG: 001 DEG 56 MIN 18,696 SEC E CONVERGENCE: - 0,54'15.564' -.9043 DEGS" "On 1998-02-04, at Well NO 15/9-19 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 6.0 hours. Operational details: RIG ON TOW TO ØLEN: POSITION 0600 HRS: N 59 DEG 02' E 003 DEG 40' SAILED DISTANCE: 61 NM DISTANCE TO PILOT POINT: 52 NM ETA AT PILOT POINT: 1800 HRS TODAY. AVERAGE SPEED 4,11 NM. PACIFIC BUCCANEER IN BRIDLE PULLING WITH 75% OF MAX POWER." "On 2007-06-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held pre-job meeting prior to start operation." "On 2007-06-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: P/U 36' hole opener BHA, hung off in rotary. Installed bushing and slips. Removed safety clamp from centralizer guide bushing. Attempted to calibrate MWD depth sensor - no sucess - decided to use drillers depth for survey reference." "On 2007-06-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: Continued making up 36' hole opener BHA." "On 2007-06-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 146m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Changed to automatic slips. RIH with 36' hole opener BHA on 5 1/2' HWDP. Dove ROV. Observed stabbing BHA into guide funnel with ROV. Tagged seabed at 145,6 m MD with no flow or rotation." "On 2007-06-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Washed down with 36' hole opener BHA with 600 lpm. Observed centralizer guide bushing landing in template guide funnel. Parked ROV in top hat prior to start rotating." "On 2007-06-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 157m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 36' hole section from 150 m to 157 m MD. Drilling parameters : Rotation 15-20 rpm / WOB 2 MT/ Flow 900 lpm. Svept hole with 15 m3 hi-vis at 157 m MD." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued drilling 36' hole section from 157 m to 170 m MD. Drilling parameters : Rotation 70 rpm / WOB 2 MT / Flow 4100 lpm / Torque 6-12 kNm . Performed survey on every single - got unreliable data at 157 m and 170 m MD." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Due to unreliable survey data and suspected inclination build up => Performed reaming trip back to 150 m MD. Meanwhile discussed situation. Found out that surveys had been taken while string was rotating which again gave wrong / unreliable readings." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Repeated survey at 170 m MD. Inclination 0,4 deg - ok." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 192m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 36' hole section from 170 m to 192 m MD. Drilling parameters : Rotation 70 rpm / WOB 2-3 MT / Flow 4100 lpm / Torque 5-8 kNm. Swept hole with 15 m3 hi-vis every single drilled. Inclination at 183 m MD 0,06 deg - ok." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 222m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Continued drilling 36' hole section from 192 m to 222 m MD. Drilling parameters : Rotation 70 rpm / WOB 2 MT / Flow 4100 lpm / Torque 8-12 kNm. Swept hole with 15 m3 hi-vis every single drilled." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 222m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Due to problems with PRS at connection - reciprocated pipe and made extra sweep with hi-vis." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 256m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Continued drilling 36' hole section from 222 to 256,5 m MD. Drilling parameters : Rotation 70 rpm / WOB 2-5 MT / Flow 4100 lpm / Torque 8-12 kNm. Swept hole with 15 m 3 hi-vis every single drilled." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 256m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated well clean with 4400 lpm / SPP 90 bar. Pumped 25 m3 hi-vis. Performed final survey at TD." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 256m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Displaced well to 1,35 sg WBM at 4000 lpm / SPP 90 bar. Pumped a total of 100 m3." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 256m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Had problems to release torque wrench when attempting to unscrew from topdrive. Troubleshot problem." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 152m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: POOH with 36' hole opener BHA from 256,5 m to 152 m MD. Topped up hole with 1,35 sg WBM pumping at 400 lpm." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued to POOH with 36' hole opener BHA from 152 m to 100 m MD. Removed automatic slips and replaced master bushing." "On 2007-06-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued to POOH with 36' hole opener BHA from 100 m to 30 m MD." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Broke out and laid out 2 single 9 3/4' DC. Attempted to rack back 36' hole opener BHA comprising of 36' hole opener, MWD and 9 3/4' DC - nogo due to exceeded weight on PRS. Hung off BHA again and broke out 9 3/4' DC. Racked back DC. Racked back hole opener / MWD." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Performed FG inspection on TDS and derrick. Vetco Gray installed inclinometer on CART bracket. Had to place shimm rings on bracket to level out the inclinometer." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Removed elevator and bails. Cleared drillfloor. Rigged up for running 30' conductor." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued rigging up for running 30' conductor. Installed bails and elevator." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Performed pre-job meeting at drillfloor prior to start running 30' conductor." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up 30' shoe joint. Filled joint with water and observed float opening - ok. Tested and rearranged tongs." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Ran 30' conductor to 66 m MD." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Ran 30' conductor including ST-2 x RL-4 xover fm 66 m to 100 m MD. Strapped top up pipe along conductor on XMT deck. Filled 30' conductor with SW on way in. Top up pipe cement outlets to be located at : 43,4 m below ML 24,5 m below ML 14,8 m below ML" "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed to 5 1/2' handling equipment prior to picking up 30' conductor housing." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up 30' conductor housing. Made up RL-4 connection to 36000 ft lbs using rig tongs. Enagaged anti-rotation slots." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 111m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran in with 30' conductor housing and installed top up pipe on XMT deck." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 111m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Installed C-plate in rotary and landed 30' conductor housing in same. Broke out and laid down 30' handling CART." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 111m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Rig up C-plate, bowl and slips for running cement stinger on top of 30' conductor housing." "On 2007-06-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 111m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Ran 4 3/4' aluminum cement stinger inside 30 conductor." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 111m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued running 4 3/4' aluminum cement stinger inside 30' conductor. Installed a total of 10 joints adding up to 91 m, i.e. approx 16 m off shoe bottom. Installed centralizers on joint number 3 and 6." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 111m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up primary CART. M/U 4 1/2' IF x butress X-over to low end of CART. M/U CART to innerstring. Removed innerstring handling equipment. Made up CART to 30' conductor housing with 5 lefthand turns. Checked inclinometer -ok. Checked filler valve in open position - ok." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Ran in with 30' conductor on 5 1/2' HWDP. Strapped residual top up pipe to the conductor housing on XMT deck. Installed ROV plugs in 30' conductor housing on Centralizer deck." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: In order not to damage ROV plugs, inclinometer and filler valve => Used chain hoists / steel slings to center top of housing through the Centralizer deck." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Ran in with 30' conductor on 5 1/2' HWDP. Observed with ROV when running through template slot." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 215m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Started loosing hook weight at 200 m MD. Worked string up and down trying to release friction in well." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 210m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Contiuned to work 30' conductor. Had overpull of 15 MT." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 237m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Closed filler valve with ROV. Started circulation with SW at 2300 lpm thorugh 30' conductor. Worked 30' conductor while circulating w/ maximum 12 bar pumppressure and 10 mt downweight. Put datum mark on pipe 112,88 m centralizer deck to top 30' conductor housing." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Broke out two joints from 5 1/2' HWDP stand. M/U cement stand with side entry sub and lotorqe valve. Continued to work 30' condcutor while ciruclating SW at 2300 lpm. Reached TD and confirmed correct depth by datum mark on pipe towards machined ring on centralizer deck." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Hooked up ROV with hydraulic reservoir to hydraulic receptacle on template. Engaged centralization rams in template funnel. Pitch and roll readings : Before engaging rams ; roll 0,04 to 0,3 / pitch 0,01 to 0,2 After engaging rams ; roll static at 0,13 / pitch static at 0,05" "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated at 2300 lpm / SPP 11 bar to confirm no leaks on plugs in conductor housing. No leaks could be observed by the ROV. Meanwhile held cementing prejobmeeting at drill floor." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Prepared for cementing conductor. Lined up and tested cement lines to 200 bar / 5 min - ok." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Pumped 75 m3 of 1,50 sg X-lite cement slurry with cement unit. Pump pressure during cement displacement 13 bar. Displacement rate 800 lpm." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced cement with seawater. Pressure rose from 20 bar to approx 35 bar during displacement indicating cement in annulus and good cement job. Pumped a total of 8,5 m3 leaving theoretical TOC at 247 m MD inside the 30' conductor." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rigged down cement hose and flushed same. Flushed manifold." "On 2007-06-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: Waited on cement to set up. Meanwhile : -Cleared and tidied rigfloor -PV on drillfloor equipment -Flushed and cleaned cement unit -Inspected seabed for cement returns - inconcluisve due to poor visiblity" "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Waited on cement to set up. Meanwhile : -PV on drillfloor equipment -FG inspection on drillfloor -Grinded down weld seam on LP riser" "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to pumping down the top up pipe." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up to pump down top up pipe. Tested line and manifold 100 bar / 5 min." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Stepped up pressure pumping at 50 l/min. Held pressure at predetermined levels : 24 bar (gauge) - ok 33 bar (gauge) - ok 39 bar (gauge) - ok At 46 bar gauge, i.e approx 53 bar (770 psi) differential, pressure bled of rapidly indicating burst disk rupture. Indications are that it is the shallowmost disk that ruptured." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Assessed situation. Conferred with shore. Decided to do remedial cement job through top up pipe. Did circulation test through cement hose / top up pipe, 50 bar / 500 lpm. Meanwhile, prepared for top up cement job." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk in mud control room prior to cement top up job." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Lined up and pressure tested cement lines to 200 bar / 5 min - ok." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Performed remedial cement job. Pumped 15 m3 of 1,56 G-cement slurry. Pump pressure during cementing 32 bar. Held pumping rate steady at 350 lpm. Displaced cement down cement hose and top up pipe with 1,1 m3 SW." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Disconnected hose and dropped release ball. Let ball drop and sheard out release sub on UWG with 176 bar. Flushed cement lines/ hose down to seabed." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Released CART from 30' conductor housing by 5 righthand turns. Pulled CART clear of template. Reading on inclinometer before releasing CART : Pitch 0,09 / Roll 0,11" "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out and racked back cementing assembly." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up TDS to string and pumped cleaning sponge through the pipe at 2600 lpm." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed Inclinometer from CART with ROV. POOH with CART and cement stinger on 5 1/2' HWDP. Installed bowl and bushing for handling 4 3/4' aluminum inner string. Broke 4 1/2' IF connection underneath CART. Racked back CART in derrick." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to retrieveng 4 3/4' aluminum inner string." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke out and laid down 4 3/4' aluminum inner string. Laid down pipe in doubles." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleared rig floor of cement stinger handling equipment." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to transerferring tension cylinders through wellhead module down to Centralizer deck." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Transfered tension cylinders for F-4 down to Centralizer deck." "On 2007-06-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Transferred tension cylinders for F-7 down to Centralizer deck. ****Operations transferred to F-12****" "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded derrick towards port to allign with slot F-4." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Held toolbox talk before skidding cantilever in longitudinal direction. Observed buckeled standpipe hose in dragchain." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Straightened standpipe hose in dragchain with chainhoists." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Skidded cantilever to slot F-4 position." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Removed weatherdeck hatch on slot F-4. Installed cantilever access stairs. Made final transverse and longitudinal adjustments to center derrick above F-4. Prepared for removing support beams on aft PRS." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Removed support beams on upper arm on aft PRS. Performed NDT inspection of PRS hoisting carriage." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.8 hours. Operational details: Worked on hatches on Weatherdeck. Removed covers on WH module decks on slot F-4. Built scaffolding/fence around F-4 on all levels. Meanwhile changed to monel dies on PRS gripper head." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Rigged up slings for installing diverter. Installed diverter, outer ring and masterbushing. Rigged down slings." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 2.8 hours. Operational details: Waited on crane to finish loading/backloading supply boat due to urgent need for supply boat going to shore. Meanwhile: -Cleared and tidied drillfloor -Dressed PS-30 with 5 1/2' die holders/dies" "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up 17 1/2' drilling BHA." "On 2007-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Made up 17 1/2' BHA according to Schlumberger instructions. Gauged bit and stabilizers. Set scribline and measured corrections on GWD and MWD. Adjusted UBHO sub in line with scribeline." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Made up x-over above NM collars. RIH with 17 1/2' drilling BHA on DC/5 1/2' HWDP. Made up and ran hydraulic jar." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 220m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: While observing with ROV, stabbed 17 1/2' BHA into 30' housing/CTS funnel. RIH with 17 1/2' BHA to 220 m MD. ROV took position and started CTS pump. Not able to operate suction valve from pit#7 when attempting to start pumping." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 220m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Not able to operate suction valve from pit#7. Locked valve open." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 250m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Commenced pumping at 3500 lpm and tested communication to MWD - ok. Observed severe cavitation in string. Reduced rate to 2000 lpm and washed down to 247 m MD and tagged TOC. Drilled cement inside 30' shoetrack. Drilling parameters : 3500 lpm / SPP 80 bar / 40 RPM / Torque 1-3 kNm / WOB 4 MT." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 260m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and opened 36' / 26' / 17 1/2' rathole from 250 m to 260 m MD. Drilling parameters : Flow 3500 lpm / SPP 82 bar / 40 RPM / WOB 1-2 MT / Torque 2-3 KNm. Reamed through shoetrack / rathole 3 times. Pumped 20 m3 hi-vis to clean hole." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 265m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled new formation from 260 m to 265 m MD. Drilling parameters : Flow 3500 lpm / SPP 83 bar / 40 RPM / WOB 1-3 MT / Torque 2-3 KNm." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 265m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pumped 15 m3 hi-vis sweep on bottom. Had to wait for WL gyro unit to become operational." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 223m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Had to wait for WL gyro unit to become purged and operational. This was caused by downtime on STB crane during the night, not able to do the lift in due time. Circulated at 3500 lpm and reciprocated pipe. Racked back stand and pulled bit inside conductor shoe to 223 m MD." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 223m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Removed masterbushing and installed automatic slips." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 262m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 17 1/2' BHA from 223 m to 262 m MD to obtain favourable stick up for running WL gyro. Not able to lay out single due to WL unit in V-door. Rigged up for running WL gyro. Held toolbox talk prior to running gyro." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 262m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: RIH with gyro on WL, located gyro in UBHO and performed survey. Pulled out with gyro and performed survey while pulling out." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 262m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Attempted to orient toolface - negative due to high torque. Pulled string to work out the torque, observed 25 MT overpull." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 262m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Attempted to pull inside shoe, observed 25 MT overpull." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Installed 5 m pup joint and made up TDS for pumping. String free down. Established circulation with 3100 lpm. Swept hole with 20 m3 hi-vis. Pulled 17 1/2' BHA from 262 m to 249 m MD inside conductor shoe. Got 11 m stick-up." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: RIH with gyro on WL, located in UBHO and performed survey. Oriented toolface as required. Halted operation due to possible power-shut down during ESD test." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 265m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 17 1/2' BHA to 265 m MD. Laid out 5 m pup joint and made up stand." "On 2007-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 424m. The activity was categorized as 'drilling -- drill' and lasted for 8.2 hours. Operational details: Drilled 17 1/2' hole section from 265 m to 424 m MD. Slided and rotated according to instructions from DD. Drilling parameters : 3500 lpm / SPP 75-90 bar / 100 RPM / WOB 1-9 MT / Torque 3-7 kNm. Increaed RPM to 140 during rotary drilling. Pumped 30 m3 hi-vis per stand to clean hole. Average ROP 19 m/hrs. Good correspondance between GWD and MWD obtained at 383 m MD." "On 2007-10-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 560m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' hole section from 424 to 560 m MD. Slided and rotated according to instructions from DD. Drilling parameters : 3500-3800 lpm / SPP 90-100 bar / 100 RPM / WOB 5-12 MT / Torque 4-7 kNm. Increaed RPM to 140 during rotary drilling. Pumped 2 x 15 m3 hi-vis per stand to clean hole. Average ROP 23 m/hrs. Performed cluster shots for SUCOP corrections of MWD data." "On 2007-10-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 866m. The activity was categorized as 'drilling -- drill' and lasted for 10.2 hours. Operational details: Drilled 17 1/2' hole section from 560 m to 866 m MD. Slided and rotated according to instructions from DD. Drilling parameters : 3500-4500 lpm / SPP 90-145 bar / 100 RPM / WOB 5-10 MT / Torque 6-9 kNm. Increased RPM to 140 during rotary drilling (string RPM 55). Pumped 3 x 10 m3 Hi-vis per stand. Reamed one single per stand. Average ROP 30 m/hrs." "On 2007-10-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 866m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Prepared for driling Utsira formation at 866 m MD. Reamed full stand once. Circulated 1,5 x bottoms up at 4500 lpm. Inclination before entering Utsira was 16,6 deg." "On 2007-10-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1107m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled 17 1/2' hole section from 866 to 1107 m MD. Top Utsira encountered at 890 m MD. Slided and rotated according to instructions from DD. Drilling parameters : 3100 lpm / SPP 90-100 bar / 100 RPM / WOB 5-12 MT / Torque 4-7 kNm. Increased RPM to 140 during rotary drilling (string RPM 55). Pumped 3 x 15 m3 Hi-vis per stand. Average ROP 37 m/hrs." "On 2007-10-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Observed negative drilling brake indicating base Utsira encontered at 1077 m MD. Drilled 17 1/2' hole section from 1077 to 1107 m MD. Inclination on base Utsira 12,3 deg." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1200m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled 17 1/2' hole section from 1107 to 1200 m MD. Slided and rotated according to instructions from DD. Drilling parameters : 3800 lpm / SPP 110-120 bar / 100 RPM / WOB 6-10 MT / Torque 6-8 kNm. Increased RPM to 140 during rotary drilling (string RPM 55). Pumped 3 x 10 m3 Hi-vis per stand. Average ROP 22 m/hrs." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1200m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Prepared for drilling Skade formation at 1200 m MD. Reamed on singel 5 m off bottom. Circulated 1,5 x bottoms up at 4500 lpm. Inclination before entering Skade formation 16,3 deg." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1202m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 17 1/2' hole section from 1200 to 1202 m MD." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled 17 1/2' hole from 1202 m MD to TD at 1360 m MD. Slided and rotated according to instructions from DD. Drilling parameters : 3100-4500 lpm / SPP 120-165 bar / 100 RPM / WOB 6-10 MT / Torque 8-9 kNm. Increased RPM to 140 during rotary drilling (string RPM 55). Pumped 3 x 10 m3 Hi-vis per stand. Average ROP 30 m/hrs." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Cleaned hole on TD. Pumped sweeps of 30 m3 hi-vis, 30 m3 seawater and 30 m3 hi-vis. Pumped 3 x bottoms up at 4500 lpm / SPP 150 bar. String RPM 60. Reciprocated full stand while pumping." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Displaced 17 1/2' hole section to 1,40 sg WBM at 4500 lpm / SSP 135-200 bar. Reciprocated full stand while pumping. Pumped a total of 225 m3 1,40 sg WBM." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 220m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 1360 m to 220 m MD. Observed thight spots at : 1345 m MD 20-30 MT overpull 1175 m MD 20 MT overpull 1145 m MD 15 MT overpull 1135 m MD 15 MT overpull 745 m MD 10 MT 690 m MD 10 mT Intervall 580 to 380 m MD 10-12 MT overpull" "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 220m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Topped up well with 40 m3 1,40 WBM. Stopped to investigate for hydraulic leak on top drive." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 220m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Investigated hydraulic leakage on TDS. Found leakage in easy accessible hose fitting. Tightened hose. Further work on TDS needed as a less accessible leakage was observed." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Removed automatic slips and installed masterbushing. Pulled 4 stands. Meanwhile prepared for repairing leakage on TDS." "On 2007-10-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Parked TDS and repaired leakage on TDS gear box system." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Repaired leakage on TDS gear box system." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Broke out and laid down 17 1/2' drilling BHA. Cleaned and tidied rigfloor." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PIcked up cement head and made up to 6,69 m 5 1/2' DP pup. Laid down cement head w/pup on deck." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Rigging for running 13 3/8' casing. Cleared and tidied drillfloor. Removed masterbushing. Rigged up slings for removing diverter." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed diverter. Installed hole cover. Rigged down slings." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tolbox talk prior to rigging casing running equipment." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Greased and checked TDS visually." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Rigged up for running 13 3/8' casing. Dressed PS-30 slips for 13 3/8'. Moved casing tong to drillfloor and set on rails, hooked up hydraulics and panel. Rigged up circulation packer, 500T slip type elevator and slings with single joint elevator. Installed PS-30 slips in rotary." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to running 13 3/8' casing." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up, made up and ran 13 3/8' shoe joint, float collar joint and 6 m pup joint. Threadlocked couplings. Filled casing with SW and tested float for flowthrough - ok." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran 1 joint of 13 3/8' casing. Adjusted torque setting on tong. Tong jammed to coupling and could not be released." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 43m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Casing tong stuck on casing coupling. Removed die carrier to release the grip." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Ran 1 joint of 13 3/8' casing. Still problems with torque setting on casing tong." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 55m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired casing tong. Changed sensor and cable. Adjusted dump valve setting." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Ran 13 3/8' casing from 55 m to 200 m MD. Filled casing with seawater. Got problems functioning PS-30 slips." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 115m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Not able to open PS-30 slips. Thightened fitting on hydraulic hose." "On 2007-10-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 380m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Ran 13 3/8' casing from 200 m to 380 m MD. Filled casing with 1,40 sg WBM every 5th joint. Average running speed 6 joints/hr." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: Ran 13 3/8' casing from 380 m to 800 m MD. Filled casing with 1,40 sg WBM every 5th joint. Average running speed 6 joints/hr." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rearranged catwalk machine to pick casing from fwd STB bay." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: Ran 13 3/8' casing from 800 m to 1198 m MD. Filled casing with 1,40 sg WBM every 5th joint. Average running speed 6 joints/hr." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging down casing running equipment." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Removed PS-30 slips and installed master bushing. Removed 500T slip elevator. Removed FAC circulation tool. Removed casing bails and installed drilling bails and 5 1/2' elevator." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up 13 3/8' x 18 3/4' subsea wellhead." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1214m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up 13 3/8' x 18 3/4' subsea wellhead and made up to 13 3/8' casing. Ran in with casing and well head to 1214 m MD and hung off in rotary." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1214m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing casing tong." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1214m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged down casing tong and panels and removed from drillfloor." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1345m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran in hole with casing and wellhead on 5 1/2' HWDP landing string from 1214 m to 1345 m MD. Circulated last stand down with 500 lpm." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1345m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up cement head with premade pup joint and made up same to landing string and TDS. Took up/down weights 219/144 MT. Broke circulation with 500 lpm and landed 18 3/4' subsea wellhead in 30' conductor housing according to Vetco instructions." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1351m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Circulated and condtioned well before cementing. Pumped at 2300 lpm. Standpipe pressure decreased from 37 bar to 20 bar after 200 m3 pumped. Prepared for pumping cement. Observed problem with mudpumps." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1351m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Inspected mudpump#1 and revealed that swab and liner needed to be changed. Questioned if mudpump #3 was ready for operation. Tested mudpump #3 and approved for operation." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1351m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Dropped ball to activate lower wiper plug. Mixed and pumped 126 m3 1,56 sg lead cement followed by 20 m3 1,92 sg tail cement. Pump rate 800 to 1200 lpm / pumping pressure 20 bar. Displaced cement line with 890 liter seawater." "On 2007-10-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1351m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released dart in cement head. Pumped 3 m3 seawater with cement unit at 1200 lpm. After pumping approx 1 m3, observed shear of upper wiper plug by 120 bar pressure peak. Closed lo-torque on cement head and lined up to pump with mudpumps." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1351m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Displaced cement with 89,5 m3 / 4080 strokes seawater at 3000 lpm. Slowed down to 1200 lpm / SPP 70 bar prior to bumping plug. Bumped plug with 140 bar and held pressure for 10 min - ok. Lined back to cement unit and bled back 940 liter before returns stopped." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1351m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Disconnected cement line. Released CART with 5 righthand turns according to Vetco instructions. Broke out and laid down cement head with pup. Put in two sponges to clean pipe." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up CART stinger 0,5 m above wellhead. Installed cover on subsea wellhead with ROV. Washed template through drillpipe and CART tool to remove cuttings. Cavitation in string made it hard for ROV to grab onto pipe. Re-positioned ROV to right below CART stinger. Stepped up rate to 4500 lpm and washed template while moving pipe with ROV. Inspected wellhead cap and template with ROV." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to pulling CART." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with CART on 5 1/2' HWDP landing string. Laid out two singles on way out. Laid out CART tool." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed vinyl guides in Centralizer end Tensioning decks. Installed tension ring on Centeralizer deck. Meanwhile started cleaning and dredging template with ROV." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk before installing spider." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Moved riser spider to drillfloor and installed same in rotary. Hooked up hydraulics." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Rigged up bolt tensioner equipment on drillfloor. Brought fairrings, bolts, guides and caps to drillflloor." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 0.8 hours. Operational details: Waited on crane due to helicopter arrival." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up the TBC/stress joint/lower pup double E." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up TBC/stress joint/lower pup double E by simultaneous lift with deckcrane and TDS. Landed double in riser spider." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Attempted to perform pre-operational checks on TBC according to Vetco instructions, NEG. Observed leakage on minireel hose for hotstab." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Observed damaged intervall on minireel hose. Cut back minireel to 150 m and reterminated fittings. Prepared 30 m excess undamaged hose for potential extension. Function tested TBC connector according to Vetco procedures." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 22m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up 2nd double D by simultaneous lift with deckcrane and TDS, brought to vertical postion. Removed handling tool on flange in rotary. Installed guided pins. Stabbed double D onto flange in rotary. Made up flange according to Bandak procedure. Tested connection to 200 bar on flange. Installed fairrings." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Prepared guidewires with ROV hooks. Built scaffolding around and removed hatches on all wellhead module levels. Removed weatherdeck hatches on F-5 og F-9. Ran guidewires and prepared wire loops in F-4 Centralizer deck opening. Ran in with riser, hooked up guidewires at Centralizer deck and ran riser and guidwires to sealevel." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 51m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up 3rd double C." "On 2007-10-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 51m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up 3rd double C by simultaneous lift with deckcrane and TDS, brought to vertical position. Removed handling tool on flange in rotary. Installed guide pins. Meanwhile ROV attempted to install VX ring on subsea wellhead. Observed grease/shadow on seal surface. Attempted to wash/flush -still visible. Brought ROV to surface in order to mount brush tooling." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Stabbed double C onto flange in rotary. Made up flange according to Bandak procedure. Tested connection to 200 bar on flange. Installed fairrings. Ran STB guidewire to template. Ran port guidewire to 40 m below sealevel. RIH with riser to 80 m MD." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up 4th double B by simultaneous lift with deckcrane and TDS, brought to vertical position. Removed handling tool on flange in rotary. Installed guide pins. Stabbed double B onto flange in rotary. Made up flange according to Bandak procedure. Tested connection to 200 bar on flange. Installed fairrings. RIH with riser to 110 m MD. Meanwhile ROV established STB and port guidewires to template eagel clamps. Brushed and cleaned wellhead seal surface with ROV." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up 5th double A by simultaneous lift with deckcrane and TDS, brought to vertical position. Removed handling tool on flange in rotary. Installed guide pins. Stabbed double A onto flange in rotary. Made up flange according to Bandak procedure. Meanwhile brought ROV to surface and installed VX ring installation tooling. Dove ROV." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 128m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Tested riser connection to 200 bar. Installed fairings. RIH with riser to 128 m MD." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 128m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing riser spiser." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed riser spider from rotary and installed master bushing. Installed lo-torque on Claxton tool and confirmed in open position. Ran Claxton tool past rotary and hung off on manual slips." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up stand of 5 1/2' DP to Claxton tool. Made up TDS to DP." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to landing riser." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Placed VX gasket on 18 3/4' subsea wellhead with ROV. Inspected guidewires." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Ran in with riser. Took up/down weight 137 MT. Attempted to land TBC conncetor on 18 3/4' wellhead - negative. Trashed VX- ring when attempting to land. Inspected wellhead and installed new VX -ring." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waited on weather for improved landing condition. Meanwhile installed coax cable between ROV unit and drillfloor to improve viewing conditions for driller." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made 2 more attempts to land TBC connector on 18 3/4' wellhead - negative. Both times the VX-ring was bounced off the wellhead. Lost attachement for 1 guidewire. Installed new VX-ring." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Landed TBC connector on 18 3/4' subsea wellhead succesfully. Set down 30 MT weight. Observed loose skirt on TBC connector." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed hotstab in TBC receptacle with ROV. Unhooked one guidewire from eagle clamp and pulled to surface. Covered open slot openings in wellhead module with hatches and removed scaffolding." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Pressured up through minireel hose to activate TBC connector in steps of 500 psi to 3000 psi. Observed indicator rods with ROV - ok. Performed overpull test on connector to 30 MT - ok. Retrieved minireel hose and 2nd guidewire to surface. Covered open slot openings in wellhead module with hatches and removed scaffolding." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Installed hatches on weatherdeck on slot F-5 and F-9." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Roped off relevant areas. Built scaffolding around slot F-4 on weatherdeck to access Claxton tool." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Adjusted tension to 20 MT overpull. Filled riser with 8,7 m3 seawater from cement unit. Closed lo-torque valve on Claxton tool. Pressure tested riser and TBC connector against the well. Pressured up to 20 bar/5 min-ok. Continued to pressure up to 145 bar - observed leakage over Claxton tool in moonpool." "On 2007-10-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure fell 20 bar over 10 min with a corresponding leakage rate of 10 l/min. Observed for leakage on TBC connector with ROV - no leakage detected. Assessed situation. Decided to move ahead with operations and confirm test at a later stage." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.5 hours. Operational details: In parallel with tenison cylinder hook-up activities : Rigged up chainhoists and attached to tension ring. Removed vinyl protector guide. Installed centralizer in Centralizer deck. Removed scaffolding and barriers at Centralizer deck. Installed boat collision stool. Made up contact ring to three lowermost groves on serrated area. Assembled tensioning assembly and made up to tension ring. Removed chainhoists. At 05:30 operations had progressed to the point where tension cylinders support was required." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Continued working on tension cylinders. Meanwhile started moving BOP from test stump to trolley." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Worked on tension cylinders." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Made up tensioning assembly to two pistions and elavated tensioning assembly to contact ring. Applied 2 x 20 MT tension. Made up the two other tension cylinders to tensioning assembly. Installed shimm ring underneath tensioning assembly." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Transferred tension from block to tension cylinders. Applied 4 x 20 MT on tension cylinders." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Broke out Claxton tool from BOP joint with Hy-torq tool. Pullled 5 1/2' landing stand, broke out same and racked back in derrick." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed master bushing. Pulled Claxton tool and laid out same. Found 1 O-ring missing on Claxton tool and 1 O-ring bursted." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to skidding BOP." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Attempted to break out 4 remaining studs on NT-2 connector - negative, not able to break studs within torque limit." "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Not able to break studs on NT-2 connector. Attempted to adjust BOP to neutral weight on the NT-2 conncetor - still not able to break studs. Torque tool socket adapter broke, repaired adapter. Traced new and more powerful adapter and used same for making/breaking. Re-made all studs in attempt to break the jammed studs. Untorqued the 4 studs in question - ok. Continued BOP nippling operation. Meanwhile : -Serviced TDS -Removed support beams on forward PRS -Tested standpipe standpipe manifold 5/10 min 20/345 bar" "On 2007-10-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Untorqued all studs on NT-2 connector. Lifted BOP off test stump and skidded to well centre." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Landed BOP on riser NT-2 profile. Made up NT-2 connector. Made up tension cylinders to BOP. Meanwhile : -Calibrated forward PRS -Modified BOP overshot joint -Tested cement/kill manifold 5/10 min 20/345 bar -Prepared BOP test tool" "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Hooked up tension cylinder to BOP. Closed shear ram an lined up for testing down well from cement unit. Meanwhile finished off testing choke manifold." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pressure tested 13 3/8' casing using seawater to 20/190 bar 5/10 min - ok. Pumped 1 m3 and bled back 1 m3. Opened shear ram." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: RIH with BOP testplug on 5 1/2' HWDP. Landed plug at 139 m MD and set down 4 MT on plug." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Closed MPR. Pressure tested BOP connector, riser, wellhead and TBC connector to 20/345 bar 5/10 mins - ok." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Function tested BOP." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: POOH with Vetco test plug on 5 1/2' HWDP and laid down same." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing diverter." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed diverter from rotary." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to installing overshot joint and diverter." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed overshot and made up to flange on BOP body." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed diverter in rotary and locked same in place.." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held time out for safety meeting with rig crew." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Continued to nipple up overshot. Removed diverter bails. Installed bushings for manual slips." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging for and testing IBOP and kelly hose." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.2 hours. Operational details: Rigged up testing swage with weco and hooked up hose. Tested upper and lower IBOP to 20/345 bar 5/10 min. Broke out swage. Checked dies on AFT PRS. Cleared V-door before picking up BHA." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up 12 1/4' BHA." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Picked up and RIH with powerdrive, hung off in slips.Made up and run in with powerdrive, powerpulse, NMDC and 8' DC double." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Held time out for safety meeting with rig crew for nigthshift." "On 2007-10-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Made up and ran in with powerdrive, powerpulse, ARCm NMDC and pony. Made up 2 x 8' DC double. Observed leakage on flange between overshot and BOP." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Laid down jar from derrick. Picked up new jar from deck and made up to BHA. Meanwhile worked to repair leaking flange. Observed that flange appeared to be biased towards one side." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Broke and thigthened bolts as required whilst levelling BOP" "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Made up 8' DC stand and x-over. Installed automatic slips in rotary. RIH with 12 1/4' drilling BHA on 4 stands of 5 1/2' HWDP to 135 m MD." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: RIH with 12 1/4' drilling BHA from 135 m MD to 600 m MD." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Ran in hole with 12 1/4' drilling BHA from 600 m to 1000 m MD. Inspected slips on PRS." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to routing SW returns overboard." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Established circulation rate at 1500 lpm. Tested MWD according to Schlumberger procedure - ok." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1300m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Ran in hole with 12 1/4' drilling BHA from 1000 m to 1300 m MD. Performed kick drill." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1336m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Made up TDS and washed down from 1300 m. Tagged cement at 1336,5 with 1500 lpm / SPP 54 bar. Took up/down weights 135/115 MT." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1336m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Conducted choke drill." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- drill' and lasted for 8.5 hours. Operational details: Drilled 13 3/8' shoetrack from 1336,5 m to 1348 m MD with seawater. Drilling parameters : Flow 2500 lpm / SPP 50-65 bar / 30-50 RPM / WOB 2-10 MT / Torque 10-27 kNm. Pumped hi-vis sweeps ." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1350m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Drilled shoetrack from 1348 m to 1350 m MD. Meanwhile held pre-job meeting before displacing well to 1,40 OBM. Emptied slurry holding tank into pit #1 and #5 to obtain more buffer for cuttings slurry. Pumped hi-vis .Displaced well from seawater to 110 m3 1,40 OBM. Stopped pumping when OBM interface at surface." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1350m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pumped 5 m3 seawter/OBM interface to pit #5. Pumped treatable interface of 10 m3 to pit #14. Filled sandtraps and shaker pits with 1,40 sg OBM. Total active volume 185 m3." "On 2007-10-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1352m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled shoetrack from 1350 m to 1351,5 m MD. Drilling parameters : Flow 2600 lpm / SPP 101 bar / 60 RPM / WOB 5 MT / Torque 6-7 kNm. Hard to make progress at 1351,5 m MD." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1352m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued drilling on shoe, hard to make progress. Reduced RPM to 40 and reduced flow to 2200 lpm. Increased WOB steadily from 5 to 7 MT and broke through shoe." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1360m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled rathole, reamead back to shoe for every 2 m drilled. Flow 2600 lpm / SPP 101 bar / 60 RPM / WOB 5 MT / Torque 6-7 kNm." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1363m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 3 m new formation prior to FIT. Circulated well to obtain even MW in and out ; 1,39 sg heavy in/out. Used 1,395 sg for FIT calculation." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1350m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Pulled bit inside casing shoe at 1350 m MD. Lined up for FIT test to pump down pipe and annulus. Closed annular. Pressured up to 7 bar to fill standpipe and kill line and observed rapid increase in pressure / curve deflection. Pumped 121 liter up to 17 bar. Pressure fell to 13 bar over 15 min, steady leakage rate. Bled back 50 liter." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1350m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: Discussed quality of FIT. Down linked MWD for ESD, got ESD figure of 1,37 sg. Decided to line up for new FIT. Circulated and lined up for new FIT." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1350m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated on well at 3500 lpm to obtain even MW in/out. Leak tested kill line to HCR to 20 bar-ok. Obtained 1,39 sg MW in/out. Racked back 1 stand." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1350m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Lined up for FIT. Reset pressure to zero bar. Pressured up to 6,5 bar at 50 lpm to fill standpipe and kill line and observed rapid increase in pressure /curve deflection. Continued pumping at 50 lpm up to FIT pressure of 18 bar. Pumped 100 liter up to 18 bar / 1,53 EMW. Pressure fell to 13 bar after 15 mins with steady leakage rate. Bled back 50 liter." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1365m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Stepped up pumps and RPM. Drilled 2 m of new formation. Took surveys and downlinked tools according to Schlumberger instruction. Downlinked and set powerdrive according to DD instructions." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1544m. The activity was categorized as 'drilling -- drill' and lasted for 7.8 hours. Operational details: Drilled 12 1/4' section from 1365 m to 1544 m MD. Drilling paramters : Flow 3500 lpm / SPP 171-178 bar / 130-170 RPM / WOB 2-4 MT / Torque 1-4 kNm. Average ROP 23 m/hrs. Reamed 1 single before connection. Took SCRs at 1504 m MD." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1544m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Inspected TDS due to excessive noise. Found worn area on upper IBOP actuator sleeve." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1585m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 1 stand from 1544 m to 1584 m MD while observing / monitoring upper IBOP actuator sleeve. Halted operations for troubleshooting." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1585m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Decided to pull 12 1/4' drilling BHA into casing shoe for TDS repair. Circulated hole clean with 2-3 bottoms up at 3500 lpm." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1585m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min - well static." "On 2007-10-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Installed mud bucket. Pulled 12 1/4' drilling BHA from 1585 m MD to 1343 m MD." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Circulated bottoms up with 2300 lpm inside shoe. Installed circulating swedge. Lined up for moinitoring well on triptank." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Dismantled IBOP assembly from TDS. Helicopter arrived at 05:00 with new upper IBOP assy." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- other' and lasted for 4.2 hours. Operational details: Assembled new IBOP." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Made up swage for pressure testing IBOP assy. Tested IBOP and connections to 20/345 bar 5 /10 min - ok. Broke out and laid out test assy." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Continued working on TDS/IBOP. Greased and serviced TDS. Installed drilling bails and tilt arm." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Held toolox talk and installed automatic slips in rotary." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1584m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: RIH with 12 1/4' drilling BHA from 1343 m to 1503 m MD. Made up TDS and washed down from 1503 m to 1584 m MD with 1700 lpm. Took up/down weight 125/117 MT." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1584m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Took MWD survey. Stepped up pump and rotation to obtain drilling parameters. Standpipe pressure fell rapidly when reaching 130 bar. Unclear indications. Attempted to pump and observed that pop off valve had triggered. Mud returns from pop off ventline went down to pit #15 which overflowed pit and pit room. Halted operation." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1584m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Mechanical pop-off valve had taken damage and nedeed to be replaced. No spare available. Blinded off line with lo-torqe valve and lined both mudpump#1 and mudpum#2 pumps to one pop-off valve. Mudpump #3 still dedicated for barite injection in spudcans. Meanwhile troulble shooting on pop-off, circulated with 800-1000 lpm and resiprocated string." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1640m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 12 1/4' section from 1585 m to 1640,5 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / 130-170 RPM / WOB 2-3 MT / Torque 10-12 kNm. Average ROP 19 m/hrs. Reamed 1 single before connection. Not able to handle cuttings return from well." "On 2007-10-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1640m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Not able to handle cuttings return from well. Conveyer screw from shakers to skip shute blocked. Still circulating on mill tank to get cuttings slurry within viscosity specification." "On 2007-10-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1640m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Continued working on unblocking the conveyor screw. Pumped DCI active volume to holding tank." "On 2007-10-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1706m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled 12 1/4' section from 1640,5 m to 1706 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / 130-170 RPM / WOB 0-2 MT / Torque 10-12 kNm / ECD 1,42. Average ROP 12 m/hrs. Drilled with reduced ROP when going directly to skips. Worked to bring down vicosity in DCI milltank/active before injecting slurry." "On 2007-10-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1750m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 12 1/4' section from 1706 m to 1750 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / 170 RPM / WOB 2-3 MT / Torque 8-12 kNm / ECD 1,42. Average ROP 12 m/hrs. Drilled with reduced ROP when going directly to skips. Worked to bring down vicosity in DCI milltank/active before injecting slurry. Changed out cooling water on MP2." "On 2007-10-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1748m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Picked off bottom due to problems with cutting shute blocking up. Circulated 2000 lpm / 65 bar." "On 2007-10-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1748m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Circulated hole clean at 1730 m with 3500 lpm / 174 bar / 30-80 rpm. While circulating, evaluated risk involved with Siemens software update on power management system during drilling operation." "On 2007-10-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1340m. The activity was categorized as 'drilling -- wait' and lasted for 12.0 hours. Operational details: Waiting on Siemens software update. Meanwhile: - Flow checked well before POOH (static). - POOH from 1750 m to 1530 m. Up weight 140 MT / Down weight 124 MT. Monitored well on trip tank at 1530 m. Ok. - POOH from 1530 to inside csg shoe at 1340 m MD. - Continued with PMs and housekeeping/cleaning. - Continued injecting cuttings into F-12 and flushed with 2 x annulus volumes of water. - Repaired Barite hopper B." "On 2007-10-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1340m. The activity was categorized as 'drilling -- wait' and lasted for 0.5 hours. Operational details: Waiting on Siemens software update." "On 2007-10-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1750m. The activity was categorized as 'drilling -- wait' and lasted for 3.0 hours. Operational details: Removed TIW valve. RIH with 12 1/4' drilling BHA from 1340 m to 1706 m MD. Made up TDS and washed down from 1706 m to 1750 m MD with 2500 lpm / 98 bar. Took up/down weight 143/121 MT." "On 2007-10-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1750m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Established parameters and downlinked tool as per DD's instruction." "On 2007-10-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1787m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' section from 1750 m to 1787 m MD. Drilling parameters : Flow 3500 lpm / SPP 187 bar / 170 RPM / WOB 2-3 MT / Torque 9-14 kNm / ECD 1,43. Average ROP 25 m/hrs. Reamed 1 single before connection. Down linked and performed surveys as required." "On 2007-10-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2178m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 12 1/4' section from 1787 m to 2178 m MD. Drilling parameters : Flow 3500 lpm / SPP 186-194 bar / 170 RPM / WOB 0-5 MT / Torque 11-13 kNm / ECD 1,43-1,44. Average ROP 35 m/hrs. Reamed 1 single before connection. Down linked and performed surveys as required. Observed erratic data on Resestivity log from 2030 mMD (2010 mMD sencor depth). Resistivity sensor non-functional from 2010 mMD at 18:00 hrs. Cuttings return routed to skips due to slurry transfer pump is out of operation." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2230m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 12 1/4' section from 2178 m to 2230 m MD. Drilling parameters : Flow 3500 lpm / SPP 194-197 bar / 170 RPM / WOB 2-7 MT / Torque 13-15 kNm / ECD 1,44. Average ROP 35 m/hrs. Reamed 1 single before connection. Down linked and performed surveys as required. Cuttings return routed to skips due to slurry transfer pump is out of operation." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2230m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed liner spray on MP#2." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2275m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 12 1/4' section from 2230 m to 2275 m MD. Drilling parameters : Flow 3500 lpm / SPP 197 bar / 170 RPM / WOB 2-7 MT / Torque 14-16 kNm / ECD 1,44. Average ROP 35 m/hrs. Reamed 1 single before connection. Down linked and performed surveys as required. Cuttings slurry routed to boat due to injection pump is out of operation." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2311m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' section from 2275 m to 2311 m MD. Drilling parameters : Flow 3500 lpm / SPP 197 bar / 170 RPM / WOB 2-5 MT / Torque 14-15 kNm / ECD 1,44. Average ROP 35 m/hrs. Reamed 1 stand before connection. Down linked and performed surveys as required." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2311m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Cleaned out water in cooling tank on MP#2. Meanwhile Picked off bottom and circulated at 1750 lpm / 55 bar / 20 RPM." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2311m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: MP#2 had to be replaced by MP#3 due to leaking swab. MP#3 had been run in test mode and charge pumpe had to be de-isolated. Meanwhile Picked off bottom and circulated and reciprocated string at 1750 lpm / 55 bar / 20 RPM." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2377m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 12 1/4' section from 2311 m to 2377 m MD. Drilling parameters : Flow 3500 lpm / SPP 200-205 bar / 170 RPM / WOB 4-7 MT / Torque 13-15 kNm / ECD 1,43-1,45. Average ROP 10-35 m/hrs. Reamed 1 stand before connection. Down linked and performed surveys as required." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2377m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Valve in cutting injection system (CRI) would not open. Hydraulic oil was drained from closing side of automatic valve to make it open. Meanwhile cleaned out cooling water on MP#3. Meanwhile Picked off bottom and circulated at 1750 lpm / 55 bar / 20 RPM." "On 2007-10-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2497m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled 12 1/4' section from 2377 m to 2497 m MD. Drilling parameters : Flow 3500 lpm / SPP 200-205 bar / 170 RPM / WOB 4-7 MT / Torque 15-20 kNm / ECD 1,43. Average ROP 35 m/hrs. Reamed 1 single before connection. Down linked and performed surveys as required. Lined over from MP#3 to MP#2 at 21:45." "On 2007-10-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2626m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled 12 1/4' section from 2497 m to 2626 m MD. Drilling parameters : Flow 3500 lpm / SPP 205 bar / 170 RPM / WOB 4-7 MT / Torque 16-18 kNm / ECD 1,44. Average ROP 35 m/hrs. Reamed 1 single before connection. Down linked and performed surveys as required. Started injecting cuttings slurry into F-12 annulus at 03:30. Turned back time 1 hour at 03:00 due 'winter-time' in Norway." "On 2007-10-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 12 1/4' section from 2626 m to 2770 m MD. Drilling parameters : Flow 3500 lpm / SPP 209-211 bar / 160-180 RPM / WOB 4-10 MT / Torque 15-22 kNm / ECD 1,43-1,44. Average ROP 1-10 m/hrs. Reamed 1 single before connection. Down linked and performed surveys as required. Started injecting cuttings slurry into F-12 annulus at 20:10." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 12 1/4' section from 2768 m to 2770 m MD. Drilling parameters : Flow 3500 lpm / SPP 203 bar / 170 RPM / WOB 7 MT / Torque 15-20 kNm / ECD 1,43. Average ROP 1-4 m/hrs." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated 2 btms up at 2770 m MD, 3500 lpm / 200 bar / 170 rpm / 13-15 kNm to clean well. Took one roadmap measurement, 200 lpm and 60 rpm. Up weight 175 MT. Down weight 156 MT." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: BO one std, RU and dropped gyro. Pumped down tool, 550 lpm / 7 bar / 15 rpm and landet off on totco ring on top off jar in BHA." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2768m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well while rotating with 10 rpm. Sat tool face on drop gyro." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2525m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Pulled first 5 stnds wet from 2768 to 2550 m MD. No drag observed. Pumped 4,7 m3 1,65 sg slug at 880 lpm / 22 bar. Continued POOH to 2525 m MD. Gyro survey was performed on each stand." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1330m. The activity was categorized as 'drilling -- drill' and lasted for 6.2 hours. Operational details: POOH with 12 1/4' BHA from 2525 m to 1330 m MD. No overpull observed. No obstruction met pulling into 13 3/8' csg shoe. Performed gyro survey on each stand. Oriented string to confirm toolface every 300 m as instructed by Gyro data. Corrected ZMS interlock fault on aft PRS." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1330m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Function tested BOP while circulated through choke and kill lines at 13 3/8' csg shoe. Serviced TDS. Flow checked before POOH with 12 1/4' BHA in casing." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: POOH with 12 1/4' BHA from 1330 m to 90 m MD. Performed gyro survey on each stand. Oriented string to confirm toolface every 300 m as instructed by Gyro data." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.2 hours. Operational details: Removed auto-slips from rotary and inserted master bushings. LO 12 1/4' BHA from 90 m to surface." "On 2007-10-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: MU up wear bushing RT assembly and RIH with same from surface to 138 m. Tool landed off at 139.05 m. Jetted BOP and wellhead, 1650 lpm / 8 bar." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with wear bushing and LO same." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MU cmt head assembly and RB in derrick." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Cleared and tidied rig floor off excess equipment. RU csg tong, handling equipment and FAC tool. Prepared to run 9 5/8' csg." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RU csg tong and handling equipment. Prepared to run 9 5/8' csg." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Sorted out power supply problem for csg. tong." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Installed elevators, flush mounted slips, bails and FAC circulating tool. Prepared to run 9 5/8' csg." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 171m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Held tool-box meeting before running csg. PU and MU shoe joint, intermediate- and float collar joints. Thread locked first 3 connections. Checked shoe and float collar for flow-through while PU. RIH with 9 5/8' csg to 171 m MD. Filled every joint with 1.40 sg mud using FAC tool." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 167m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Casing torque computer would not work according to set up. Had to continue with modified set-up." "On 2007-10-30, at Well NO 15/9-F-4, a drilling event occurred at a depth of 276m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 9 5/8' csg from 171 to 276 m MD. Filled every joint with 1.40 sg mud using FAC tool. First 19 joint was ran with centraliser." "On 2007-10-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 416m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 9 5/8' csg from 276 to 416 m MD. Filled every joint with 1.40 sg mud using FAC tool." "On 2007-10-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 393m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Changed proximity switch on PDM." "On 2007-10-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 587m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 9 5/8' csg from 416 to 587 m MD. Filled every joint with 1.40 sg mud using FAC tool." "On 2007-10-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1550m. The activity was categorized as 'drilling -- casing' and lasted for 18.0 hours. Operational details: RIH with 9 5/8' csg from 587 to 1550 m MD. Filled every joint with 1.40 sg mud using FAC tool. LO 3 jnts. Running speed 4-7 jnts/hr." "On 2007-11-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1858m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 9 5/8' csg from 1550 to 1858 m MD. Filled every joint with 1.40 sg mud using FAC tool. Average running speed 4-5 jnts/hr." "On 2007-11-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2151m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: RIH with 9 5/8' csg from 1858 to 2151 m MD. Filled every joint with 1.40 sg mud using FAC tool. Average running speed 4-5 jnts/hr." "On 2007-11-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2151m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: PU and installed 9 5/8' x 10 3/4' XO. Changed to 10 3/4' inserts in elevator and slips." "On 2007-11-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2369m. The activity was categorized as 'drilling -- casing' and lasted for 6.2 hours. Operational details: RIH with 10 3/4' csg from 2151 to 2369 m MD. Filled every joint with 1.40 sg mud using FAC tool. Average running speed 4-5 jnts/hr." "On 2007-11-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2369m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Performed maintenace on flush joint elevator. Changed dies in csg tong. Meanwhile repaired camera on PDM." "On 2007-11-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2574m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: RIH with 10 3/4' csg from 2369 to 2574 m MD. Filled every joint with 1.40 sg mud using FAC tool. Average running speed 4-5 jnts/hr." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2617m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 10 3/4' csg from 2574 to 2617 m MD. Filled every joint with 1.40 sg mud using FAC tool. Average running speed 4-5 jnts/hr. Up weight 261 MT / Down weight 193 MT." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2617m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RD FAC tool and changed bails. Changed to 5 1/2' HWDP hadling equipment." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2626m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: PU and MU 10 3/4' casing hanger / PADPRT assembly. Marked running tool to make sure it is not backing out. Took out master bushing and ran hanger assy through rotary. Re-installed master bushing. Removed csg tong." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2698m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 10 3/4' x 9 5/8' csg on 5 1/2' HWDP landing string from 2626 to 2698 m MD." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2740m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 10 3/4' x 9 5/8' csg on 5 1/2' HWDP landing string from 2698 to 2740 m MD." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2740m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: PU cement head and broke circulation in steps up to 2000 lpm, 500 lpm=20 bar and 2000 lpm=56 bar" "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH slowly and landed off hanger. Observed 10 MT drag prior to landing off. Pumped 500 lpm and observed weight dropped off." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Circulated 1 csg volume with 1.40 sg OBM at 200 lpm / 57 bar. Meanwhile hed pre-job meeting for cmt job." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up and pressure tested cmt line 245 bar / 5 min. Verified correct line-up by holding and releasing 10 bar through low torque." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped 10 m3 base oil and 20 m3 spacer at 2000 lpm / 48 bar. Mixed and pumped 17,3 m3 1.90 sg cement slurry at 800 lpm / 40-45 bar." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pumped 490 ltrs water, released dart and continued pumping 400 ltrs water behind cement with cmt unit, to displace surface line volume to rig floor. Zeroed stroke counters for mud pumps. Displaced and sheared wiper plug by pumping OBM at 1200 lpm using rig pumps. Wiper plug sheared at 138 bar / 886 ltr. Continued displacing cement with 102.8 m3 OBM at 2000 lpm using mud pumps. Slowed down rate to 1000 lpm / 33 bar (FCP) approx 4 m3 prior to bump. Bumped plug with 110 bar after pumping 4718 strokes, which gives a pump efficiency of 95.3%." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Bled off pressure to 20 bar and closed IBOP. Equalized pressure and opened lo-torque valve. Pressured up well to 310 bar / 10 min through lo-torque valve to test casing. 1300 ltrs pumped and got 1350 ltrs back. Bleed off and checked for back flow to cmt unit. Disconnected cmt hoses and flushed lines." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up top drive to trip tank to monitor returns. Tested surface lines against fail safe valve to 207 bar / 10 min. Closed upper pipe ram and applied 207 bar to set seal assembly." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Took 40 MT overpull. Attempted to pressure test seal assembly without sucess." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Released PADPRT, LO cement head and 2 jnts of 5 1/2' HWDP. POOH with running tool on 5 1/2' HWDP landing string from 120 m to OOH." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RIH with BOP test plug to 139 m to test MS seal. Closed upper pipe ram. Attempted to pressure test seal assembly to 35 bar / 5 min without sucess. Closed annular to test upper pipe ram and found that upper pipe ram was leaking. Closed lower pipe ram and pressure tested seal assembly to 35 bar / 5 min and 345 bar / 15 min. 463 ltrs pumped and got 450 ltrs back. POOH with BOP test plug." "On 2007-11-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH and installed wear bushing at 139 m MD." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with wear bushing running string." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- other' and lasted for 4.2 hours. Operational details: RIH with 7 stds of 5 1/2' DP. MU and RIH with 10 3/4' RTTS with storm valve on 5 1/2' DP to 350 m MD. Up weight 91 MT / Down weight 87 MT. Weight under RTTS is 10.2 MT (bouyant)." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- other' and lasted for 0.7 hours. Operational details: Resiprocated string and circulated with 100 lpm to clean setting area. Installed plug according to Halliburton procedure with element at 350 m MD. Lined up to test RTTS to 180 bar/10 min from below." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 349m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Tested RTTS packer to 180 bar / 10 min from below." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 349m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Released from RTTS with 22 turns to the left. PU from 349 m to 332 m and spaced out tool joint below LPR. Tested RTTS packer to 180 bar / 10 min from above against closed lower pipe ram." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH with RTTS running tool assembly from 332 m to 348 m MD. Circulated 1 x btms up, 2000 lpm / 11 bar." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Held pre-job meeting prior to displacing well to SW. Lined up and flushed surface lines and choke & kill hoses. Displaced well above RTTS to SW, 2000 lpm / 12 bar. Used 10 m3 baseoil as spacer." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH with RTTS running tool assembly from 348 m." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: MU jetting sub and RIH to jet BOP, 2000 lpm / 9 bar / 10 rpm. POOH with jetting tool and LO same." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Took time-out for safety to investigate doghouse being hit by unidentified projectile. Ascertain that dowel pin on dog collar sheared off and struck window at high speed." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: RIH to 28 m. MU side entry sub and TIW. Closed annular. Pumped air through choke line and displaced riser contents to trip tank. RD side entry sub and TIW. POOH from 28 m." "On 2007-11-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: Held tool box meeting prior to ND diverter. Removed elevators and RU for pulling diverter. Pulled diverter to rig floor. Removed and secured diverter housing on pipe set-back. ND and pulled slick joint." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Removed BOP tension cylinders and sat BOP on test stump." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: RU handling equipment for running Claxton tool and PU tool. Removed master bushing. Run in with Claxton tool and re-inserted master bushing." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Run in and MU Claxton tool to NT2 connector on HPDR BOP joint. MU claxton tool lock-dogs to min 1000 lf.lbs torque with air-operated tool." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 18m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Untorqued bolts on HPDR BOP joint at X-mas tree level using Bandak tool, but left bolts in flange." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 12.0 hours. Operational details: Performed house-keeping and cleaned drill-fllor, cantiliver, pump room and sack store. Meanwhile performed testing of production systems. Experienced black-out from 11:28 to 12:20." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed hand-over and held tool box meeting before pulling HPDR BOP joint." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Software problems due to black-out. Could not operate break on draw work." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Disconnected HPDR BOP joint. Removed master bushing. POOH with Claxton tool and HPDR BOP joint and re-inserted master bushing. LD claxton tool and riser joint. Installed protector on BOP riser joint flange." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed handling tool/flange on top of HPDR tension joint at X-mas tree deck." "On 2007-11-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Removed scaffolding in moonpool." "On 2007-11-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Continued removing scaffolding in moonpool and on X-mas tree deck. Installed hatch on F-4" "On 2007-11-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 4.0 hours. Operational details: Started changing wires on aft PRS. Meanwhile prepared for skidding rig to F-14." "On 2007-11-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 5.0 hours. Operational details: Continued changing wires on aft PRS. Meanwhile prepared for skidding rig to F-14 and cleaned pits. Operation continues on F-14." "On 2008-02-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.0 hours. Operational details: Prepared for skidding. Simultaneously pressure tested the rig manifold and changed out riser tension cylinder." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Continued preparing for skidding. Simultaneously pressure tested the rig manifold and changed out riser tension cylinder." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Held tool box talk prior to skidding of the cantilever." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded cantilever from F-12 to F-4." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Continued changing out tension cylinder on riser. Simultaneously pressure tested the rig manifold." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 9.5 hours. Operational details: Changed out the two remaining tension cylinders on F-4 riser. Simultaneously pressure tested stab-in valves to 345 bars. Prepared for slip and cut ." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Slipped and cut drill line. Re-calibrated block and checked the crow O-matic. Simultaneously nippled down the riser lifting sub." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Continued nippling down the riser lifting sub. Checked the torque on the Claxton riser handling tool, prior to lifting in same with the HP riser BOP joint attached." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk prior to remove the master bushing, outer ring and the hatch cover on F-4." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Retrieved the riser lifting sub, and laid out same. Cleared drill floor. Prepared for picking up the HP riser BOP joint." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to install the HP riser BOP joint." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Removed master bushing and ran with the HP riser BOP joint and landed same. Installed master bushing. Made up the HP riser BOP joint." "On 2008-02-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Built scaffolding around the HP riser BOP joint in the Moon Pool." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued building scaffolding around the HP riser BOP joint in the Moon Pool." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Released the Claxton tool. Removed master bushing, pulled the Claxton up to the Drill Floor. Installed the master bushing." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Moved the BOP into well centre. Simultaneously prepared the diverter and slick jnt on the Drill Floor." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk with new crew prior to continue nippling up the BOP and diverter." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Position the BOP and commenced making up the tension cylinders to BOP." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Made up BOP tension cylinders." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to remove the master bushing and installation of the overshot and landing the diverter." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Removed the master bushing and installed the overshot and landed the diverter. Made up the NT2 connector. Meanwhile rigged down the diverter handling equipment." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.8 hours. Operational details: M/U BOP test cup assy. and RIH with same to 139 m." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Held tool box talk prior to perform BOP test as MC procedure." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 6.2 hours. Operational details: Performed BOP test as MC procedure, 20/345 bars 5/10min." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Torqued up slip joint. Fault of middle pipe variable 3½' x 5½' rams pressure test." "On 2008-02-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Drained the riser. Opened middle variable 3½' x 5½' pipe rams and removed the rubbers." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Job suspended due to priority F12. Drilling dep. transported production Co-flex hose support frame to X-mas tree deck, through Moon Pool." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: Installed new variable 3½' x 5½' pipe rams rubbers." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Attempted to pressure middle variable 3½' x 5½' pipe rams." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Drained and opened middle variable 3½' x 5½' pipe rams. Opened top wear plate ." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Removed top wear plate and inspected seals. No visible damaged on the seals. Simultaneously serviced aft PRS." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.0 hours. Operational details: Changed out O-ring and top wear plate. Installed rams and closed doors. Simultaneously serviced aft PRS and TDS." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Pulled up test plug and laid out 3m pup and one joint. Made up one double and ran in with same and landed of the test cup at 139 m. New test area for the middle pipe rams." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Lined up the CMT unit and flushed the lines." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Pressure tested the BOP middle pipe rams 20/345 bars 5/10 min." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: Performed accumulator test." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: Retrieved the test plug and laid out same." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Made up the RTTS retrieving tool." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held tool box talk prior to displacethe well above the RTTS plug to OBM." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 342m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: RIH with RTTS retrieving tool and tagged the RTTS plug at 342m, picked up 2m." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Displaced the well above the RTTS plug to 1.40 OBM, 1500/1000 lpm." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Took up/down weight 82/79 MT. Stung into the RTTS plug, turned DP 22 turnes and torque up to 2000 ft/lbs, no pressure built up. Lined up to the trip tank. Pressure up DP to 5 bars and confirmed sufficiently engaged to tool. Attempted to release the RTTS plug by pulling 105 MT equivalent to 15 MT over pull." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Closed annular and applied 40 bars to the annulus, to collapse the hydraulic slips. Held pressure for 5 min. Bled off pressure in the annulus and opened the annular." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Picked up string in 5 MT staged from 81 MT to 115 MT. At 115 MT , equivalent to 25 MT over pull. RTTS plugs mechanical slips disengaged." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Waited for element to retract." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: POOH from 350 m to 340 m with drag of 12 MT. Pulled out wet." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Changed to PS21 slips." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 300m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: POOH from 340 m to 300 m with drag of 12 MT. Pulled out wet." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 300m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Made up to TDS. Attempted to pump down the DP, w/ 23 bars 400 litres. No returns up annulus." "On 2008-02-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 300m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took time out and evaluated situation." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Continued POOH with RTTS plug from 300 m to 140 m, pulled out wet. As comming out of the sub sea well head, lost 12 MT on the weight." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Established levels by filling the well via trip tank." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Continued POOH with the RTTS plug from 140 m to 40 m, pulled out wet. Displacement over trip tank OK." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Made up to TDS, established returns at 38 bars. POOH from 40 m to surface with the RTTS plug." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed to manual slips." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Laid out the RTTS plug. Found cement on top of the hydraulic slip. The retrieving tool was not fully entered, 5 turns out. Packing element damaged in the bottom part." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Continued POOH with 7 std of 5½' DP below the RTTS plug, from 280 m to surface." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Cleaned and cleared the drill floor. Simultaneously flushed lines from CMT unit to BOP. Commenced pressure testing of the shear rams to 20/310 bars 5/10 mins." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Cleaned and cleared drill floor and prepared for handling the 8½' drilling BHA. Meanwhile completed the pressure test of the shear rams to 20/310 bars 5/10 mins, 2.1m³ pumped 2m³ in return." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up and M/U 8½' drill BHA." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: M/U 8½' drilling BHA as per Schlumberger DD&MWD. Installed radio active sources." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 937m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: RIH with 8½' drill BHA on 5' DP, from surface to 937m." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 937m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Changed over to 5½' handling equipment." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 937m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: M/U to TDS and tested the MWD at 1500 lpm 138 bars." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2619m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Continued RIH with 8½' drill BHA on 5½' DP, from 937m to 2619m, filled every 1000m. Average RIH speed 420 m/hr." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Took weight at 2619m. M/U to TDS and washed down to 2632m, 10 rpm, 10kNm, 1500 lpm, 139 bars." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Performed choke drill with day shift." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Performed choke drill with night shift. Observed saver sub required change out" "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2632m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held tool box talk prior to change out the saver sub." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2632m. The activity was categorized as 'interruption -- maintain' and lasted for 2.8 hours. Operational details: Changed out the saver sub." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: P/U one 5½' DP std. and prepared for drilling. Found discrepancy in depth." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Counted the 5½' DP in derrick. Changed depth from 2671m to 2632m." "On 2008-02-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2670m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Washed down from 2632m to 2670m. Washing parameters : Flow 1500 lpm / SPP 140 bar / String RPM 30 / Bit RPM 146. ROP 30-40 m/hr." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2733m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued washing down from 2670m to 2733m. Washing parameters : Flow 1500 lpm / SPP 140 bar / String RPM 30 / Bit RPM 146. ROP 30-40 m/hr." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2734m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled out float. From 2733m to 2734m. Drilling parameters : Flow 1500 lpm / SPP 140 bar / String RPM 10-30 / Bit RPM 125-145. ROP 1-40 m/hr, WOB 1-9 MT. Recovered rubber at the shakers." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2751m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled shoe track from 2734m to 2751m. Drilling parameters : Flow 1500 lpm / SPP 140 bar / String RPM 30 / Bit RPM 146 / ROP 30-40 m/hr / WOB 1 MT / TQ 10-12 kNm. MUD weight 1.4 SG. Back reamed to float with 1500 lpm, RIH and made connection at 2751m, volume pumped prior to connection 26m³." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled shoe track from 2751m to 2760m. Drilling parameters: Flow 1500 lpm / SPP 140 bar / String RPM 30 / Bit RPM 145 / ROP 30-40 m/hr / WOB 1-4 MT / TQ 10-12 kNm. MUD weight 1.4 SG." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2761m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled shoe from 2760m to 2761m. Drilling parameters: Flow 1500 lpm / SPP 140 bar / String RPM 30 / Bit RPM 145 / WOB 1-6 MT / TQ 10-12 kNm." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2771m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Cleaned out rat hole from 2765m to 2771m. Cleaning parameters: Flow 1500 lpm / SPP 140 bar / String RPM 30 / Bit RPM 145 / WOB 1-3 MT." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2774m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled new formation from 2771m to 2774m. Drilling parameters: Flow 1500 lpm / SPP 140 bar / String RPM 30 / Bit RPM 145 / WOB 5-7 MT / TQ 12-14 kNm. MUD weight 1.4 SG." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Pulled back into the shoe. Racked back one std. Installed side entry sub and CMT hose. Confirmed line up from CMT unit to drill floor. Leak tested line to 100 bars 10 min." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2760m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Performed FIT test. Closed annular. Applied 64 bars down DP and ANN equivalent to 1.65 SG. Rigged down CMT hose and side entry sub." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2854m. The activity was categorized as 'drilling -- drill' and lasted for 9.0 hours. Operational details: Linked down the Power Drive. Drilled new formation from 2774m to 2854m. Drilling parameters: Flow 2070 lpm / SPP 250 bar / String RPM 30 / Bit RPM 190 / WOB 7-9 MT / TQ 16-19 kNm. ECD 1.51 SG. MUD weight 1.4 SG. Took survey before connection." "On 2008-02-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2917m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled new formation from 2854m to 2917m. Drilling parameters : Flow 2070-2090 lpm / SPP 245-250 bar / String RPM 40 / Bit RPM 203 / ROP 16-20 m/hr / WOB 7-9 MT / TQ 18-19 kNm. ECD 1.51 SG MUD weight 1.4 SG. Took survey before connection." "On 2008-02-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2993m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled new formation from 2917m to 2993m. Drilling parameters : Flow 2070 lpm / SPP 245-255 bar / String RPM 40 / Bit RPM 203 / ROP 21-23 m/hr / WOB 6-11 MT / TQ 18-21 kNm. ECD 1.51 SG MUD weight 1.4 SG." "On 2008-02-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2993m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Took survey at 2993 m MD equivalent to 2795 m TVD. Stopped drilling for further instruction in conjunction with F12 perforation and start production." "On 2008-02-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2992m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Cleaned out well reciprocating the pipe, flow 2090 lpm / SPP 215 bar / String RPM 50 / Bit RPM 213. Operations transferred to F-99." "On 2008-02-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3035m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Tagged bottom at 2993m. Drilled from 2993m to 3035m. Increased mudweight from 1.40 sg to 1.45 sg . Drilling parameters: Flow 2090-2225 lpm / SPP 200-220 bar / String RPM 180 / ROP 2.5-8,5 m/hr / WOB 4-6 MT / TQ 15-20 kNm / ECD 1.59 SG. Had heavy stick slip with 10 MT WOB to start with, reduced WOB to 5 MT." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling from 3035m to 3040m. Drilling parameters: Flow 2225 lpm / SPP 220 bar / String RPM 180 / ROP 5-6.5 m/hr / WOB 4-6 MT / TQ 18 kNm / ECD 1.59 SG. Hidra started at 3040m." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3064m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Continued drilling from 3040m to 3064m. Drilling parameters: Flow 2225 lpm / SPP 220 bar / String RPM 180 / ROP 3-6.5 m/hr / WOB 4-6 MT / TQ 15-18 kNm / ECD 1.59 SG. Held pit drill." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 8 1/2' hole section from 3064 m to 3070 m MD. Drilling parameters : Flow 2200 lpm / SPP 220 bar / String RPM 180 / WOB 3-8 MT / Torque 11-22 kNm / ECD 1,59-1,60 sg. Controlled WOB and ROP due to stick slip tendencies. Observed drilling break at 3070 m MD." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Observed drilling break at 3070 m MD, ROP increased from 5 to 30 m/hr. Flowchecked well - ok - well static." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3095m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Continued drilling 8 1/2' hole section from 3070 m to 3095 m MD. Drilling parameters : Flow 2200 lpm / SPP 220 bar / String RPM 180 / WOB 3-8 MT / Torque 15-20 kNm / ECD 1,59-1,60 sg. Controlled WOB and ROP due to stick slip tendencies." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3095m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Observed drilling break at 3095 m MD, ROP increased from 5 to 35 m/hr. Flowchecked well - ok - well static." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3103m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 8 1/2' section from 3095 to 3103 m MD. Drilling parameters : Flow 2200 lpm / SPP 222 bar / String RPM 180 / WOB 4-8 MT / Torque 16-24 kNm / ECD 1,60 sg." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3103m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed SCR's." "On 2008-02-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3265m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: Continued drilling 8 1/2' hole section from 3103 m to 3265 m MD. Added LCM materials to mud prior to entering reservoir. Drilling parameters : Flow 2200 lpm / SPP 220-231 bar / String RPM 180 / WOB 3-8 MT / Torque 11-20 kNm / ECD 1,61-1,62 sg. ROP 10-30 m/hrs. Observed top of Hugin reservoir on logs 3250 m MD / 2987 m TVD. Max gas at top reservoir lag depth 5 %. Performed pit drill at 16:25 hrs. Good response from loggers and driller." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3302m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 8 1/2' hole section from 3265 m to 3302 m MD. Drilling parameters : Flow 2200 lpm / SPP 220-231 bar / String RPM 180 / WOB 3-8 MT / Torque 11-20 kNm / ECD 1,62-1,63 sg. ROP 30 m/hrs. Max gas 6%" "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3302m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Observed increase in active of ~1 m3 over 5 mins. Flowcheked well on trip tanks - ok - well static. Found that degassers had been started - volume from sandtraps overflowed into active." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3327m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Continued drilling 8 1/2' hole section from 3302 m to 3327 m MD. Drilling parameters : Flow 2100-2200 lpm / SPP 216-238 bar / String RPM 180 / WOB 3-8 MT / Torque 11-20 kNm / ECD 1,61-1,63 sg. Limited ROP to and cut back flowrate to 2100 lpm due to increasing ECD. Downlinked powerdrive to stop build. Got problems with mudpump#2 and mudpump#3." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3327m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot mudpumps. Not able to start mudpump #3. Mudpump #2 gave wrong output on stroke setting. Decided to drill ahead using mudpump #1 only." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3346m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued drilling 8 1/2' hole section from 3327 m to 3346 m MD. Drilling parameters : Flow 2100 lpm / SPP 214 bar / String RPM 180 / WOB 3-6 MT / Torque 21 kNm / ECD 1,61 sg. ROP 30 m/hrs." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3385m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 8 1/2' hole section from 3346 m to 3385 m MD. Drilling parameters : Flow 2100 lpm / SPP 220 bar / String RPM 180 / WOB 2-5 MT / Torque 20-23 kNm / ECD 1,61-1,62 sg / ROP 20-30 m/hrs." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3385m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed SCR's." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3510m. The activity was categorized as 'drilling -- drill' and lasted for 9.0 hours. Operational details: Continued drilling 8 1/2' hole section from 3385 m to section TD at 3510 m MD. Drilling parameters : Flow 2100 lpm / SPP 220 bar / String RPM 180 / WOB 3-12 MT / Torque 13-23 kNm / ECD 1,59-1,60 sg / ROP 10-30 m/hrs. Racked back one stand of drillpipe." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3507m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Circulated hole clean with 3 x bottoms up. Reciprocated stand while pumping. Parameters : Flow 2100 lpm / SPP 212 bar / String RPM 150-180. Observed clean shakers after 3 x bottoms up." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3507m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Took up down weight 195/149 MT. Recorded off bottom torque at 10/15/20 RPM - 14-16 kNm. Sent downlink to set LWD tools according to Schlumberger instructions." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3507m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well - well static. Meanwhile held toolbox meeting prior to POOH." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3307m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pulled 5 stand wet from 3507 m to 3307 m MD. Pulling speed ~10 m/min. No overpull observed." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3307m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well - well static. Pumped 5 m3 1,65 sg slug." "On 2008-02-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2780m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 3307 m to 2780 m MD." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2740m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 2780 m to 2740 m MD inside 9 5/8' casing shoe. Recorded up down weight 163/137 MT. Recorded torque at 20 RPM - 7 kNm." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2754m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well -well static. Meanwhile inspected and serviced TDS. Dropped 2 3/4' drift with pigtail in drillpipe." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1331m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 8 1/2' drilling BHA on 5 1/2' DP from 2754 m to 1331 m MD." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1331m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Broke out x-over. Changed from 5 1/2' to 5' handling equipment. Re-inserted 2 3/4' drift into 5' DP as it would not pass the x-over." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 8 1/2' drilling BHA on 5' DP from 1331 m to 110 m MD." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed PS-21 slips. Inserted masterbushing and bowls. Worked to free 2 3/4' drift which was stuck in jar." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 53m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Freed 2 3/4' drift. Racked back jar/HWDP and 1 stand of 5' HWDP." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 53m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to laying out LWD/MWD/drilling assemblies." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Broke out and laid down NM HWDP. Removed RA-source. Broke out and laid down Isonic, Telescope, Ecoscope and Powerdrive." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned and tidied drillfloor." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 0.2 hours. Operational details: General muster alarm. Crews mustered according to list. Non critical alarm." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued to clean and tidy drillfloor. Meanwhile changed rollers for IBOP actuator on TDS." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Prepared for picking up 5 1/2' DP from deck. Meanwhile -Moved power rollers on cantilever -Prepared for running WL -Inspected, cleaned and greased PS-21 slips" "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to inspection and service on AFT PRS." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Inspected and serviced AFT PRS. Found loose bar (54 cm / 560 g) sitting in hoses/junction box below upper drive." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Evaluated finding. Suspected drag chain in PRS beam." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Inspected drag chain in PRS beam. Could not identify bar (FG) comming from PRS beam." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed derrick inspection from PRS to crown block." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.8 hours. Operational details: Removed lid and inspected inside PRS upper drive. Found rotational dragchain in AFT PRS upper drive to be damaged. Identified origin of loose bar (FG) to be cross member in rotational dragchain. Assessed damage. Decided to perform repair of dragchain." "On 2008-02-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Repaired rotational dragchain in AFT PRS upper drive. Meanwhile : -Built cable head for WL -Laid out MDT tools -Rigged load sensors on WL unit" "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Repaired rotational dragchain in AFT PRS upper drive. Meanwhile tested MDT tools" "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Repaired rotational dragchain in AFT PRS upper drive. Temporarily halted testing of MDT tools due to loading of drillpipe onto cantilever/pipe-deck." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Repaired rotational dragchain in AFT PRS upper drive. Meanwhile tested MDT tools." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.8 hours. Operational details: Tested MDT tools. Calibrated weight sensor. Brought WL rigging equipment to drillfloor." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.8 hours. Operational details: Rigged up sheaves and cable. Brought logging tools to drillfloor." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up logging string." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Made up MDT toolstring." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Tested MDT tools on surface prior to RIH." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Re-positioned lower sheave due to unfavorable cable allignment." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: RIH with MDT logging string on 7/48 cable. Perfomed shallow test - negative." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH with MDT logging tools. Performed checks on surface - ok." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.8 hours. Operational details: RIH with MDT logging string on 7/48 cable from surface to station #1 at 3245 m MD. Correlated MDT tool. Attempted to activate MDT probe - negative." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2671m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Pulled MDT tool from 3245 m to 2671 m MD inside 9 5/8' casing shoe. Troubleshot tool failure - negative." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: POOH with MDT logging string on 7/48 cable from 2671 m MD to surface." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Checked cable, cable head and surface cables - ok." "On 2008-02-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Isolated and checked MDT string components as required." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 0.5 hours. Operational details: General alarm - crews mustered according to list. Announced possible gas in wellhead area. Removed WL toolstring from well - well stable - stood by for securing well. Investigated alarm and found fault on gas sensor. Resumed work." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.8 hours. Operational details: Continued isolating and checking MDT string components as required." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Found both MRPO pumps in MDT toolstring to be faulty. Only one back up MRPO pump available on rig. Discussed situation. Decided to run simplified string with only 1 pump." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: Traced tools for simplifed MDT toolstring. Brought tools to drillfloor. Made up and tested simplified MDT toolstring." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with simplified MDT toolstring on 7/48 cable." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2700m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: RIH witth MDT toolstring on 7/48 cable from surface to 2700 m MD inside 9 5/8' shoe. Rested MDT toolstring for 30 min to allow for temperature adaption." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3270m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RIH with MDT toolstring on 7/48' cable from 2700 m to 3270 m MD." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Correlated toolstring and placed MDT probe at 3245 m MD sample point in Heather." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.2 hours. Operational details: Obatined pressure point sample at 3245 m MD in Heather. Attmepted to RIH - cable stuck with MDT at 3345 m MD." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: Worked MDT toolstring and found string to be stuck. No tension on cable head observed when pulling surface tension of max pull 12000 llbs - wire probably stuck/keyseated in formation. Depth on mechanical counter 3233 m MD." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'interruption -- fish' and lasted for 1.8 hours. Operational details: Continued to work WL with max 12000 lbs pull. Observed movement of WL unit. Secured WL unit with chains. Checked sheave wheels on drillfloor." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: Put 12000 lbs tension in WL and put on brake. Depth on mechancial counter 3232 m MD with 12000 lbs tension." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'interruption -- fish' and lasted for 7.5 hours. Operational details: Worked WL several times. Slacked off to 5000 lbs and picked up to max tension 12000 lbs several tiems - not able to make progress. Prepared for doing cut and thread fishing on drillpipe. Prepared fishing procedure. Decided to do fluid sampling at stuck point in Heather prior to fishing." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Pumped to clear tool of mud. Activated MDT probe." "On 2008-02-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Stepped up MDT pump in increments. Performed MDT sampling at 3245 m MD according to Schlumberger procedure." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: Perfomed MDT sampling at 3245 m MD. Observed 170 bar diff pressure over probe. Filled 2 ea 450 cc bottles with formation fluid. Contamination ~13%. Total volume pumped ~30 litres." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Worked WL up and down in attempt to get free - negativ. Ran probe out/in and re-attempted freeing WL - negative. Slacked off WL to 3000 lbs tension => depth on mechanical counter 3245 m MD." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to rigging up for cut and thread fishing." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3245m. The activity was categorized as 'interruption -- fish' and lasted for 2.8 hours. Operational details: Put 7200 lbs tension on WL. Fitted T-clamp on 7/48 cable and slacked off WL. Cut 7/48 cable with 5-6 m loose end and fitted spear on same. Fitted spearhead overshot and 2 x fishing weights to winch side of wireline. Removed sheave wheel from TDS. Removed sheave wheel from aft samson post." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 2.8 hours. Operational details: Rigged up for cut and thread fishing. Suspended upper sheave in dedicated sling in derrick. Suspended lower sheave in V-door above HTS, secured same with slings." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to performing cut and thread." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Picked up singel and made up x-over. Laid out single." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.2 hours. Operational details: Held toolbox talk prior to inserting PS-30 automatic slips." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 2.2 hours. Operational details: Rigged up and changed to PS-30 automatic slips. Slacked off wire and hung off in slips with T-bar." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Pull tested T-bar. Performed toolbox talk for continuation of operations." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Re-set grip on T-bar in order to get more slack on wire and be able to lay grapple/drain sub on the drilfloor. Ran WL up/down to test counter balance weights on wire - ok. Threaded first joint." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 13m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Picked up first joint. Made up grapple and drain sub. RIH with 5 1/2' DP single." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 13m. The activity was categorized as 'interruption -- fish' and lasted for 2.8 hours. Operational details: Observed damage on cable due to unfavorable angel when spinning in the drilpipe, wire partly cut through. Suspended WL in C-plate and cut off damaged wire. Fitted spearhead and fishing weights on winch side of wireline." "On 2008-02-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 13m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: Rigged down upper sheave. Attached upper sheave in crown block. Removed 5' weco coupling and blind cap on top of TDS. Put on weco nut acting as wear bushing. Threaded WL through topdrive." "On 2008-02-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 268m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: Ran 5 1/2' DP singles over 7/48 wireline from 13 m to 268 m MD according to cut and thread procedure." "On 2008-02-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 780m. The activity was categorized as 'interruption -- fish' and lasted for 9.2 hours. Operational details: Ran 5 1/2' DP singles over 7/48 wireline from 268 m to 780 m MD according to cut and thread procedure. Laid out singles #26 and #28 due to stuck protectors." "On 2008-02-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 780m. The activity was categorized as 'interruption -- fish' and lasted for 3.8 hours. Operational details: Laid out 5 1/2' DP singles on pipedeck. Measured and drifted joints. Simultaneoulsy re-arranged stands in derrick." "On 2008-02-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 780m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to continuing cut and thread." "On 2008-02-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1090m. The activity was categorized as 'interruption -- fish' and lasted for 4.5 hours. Operational details: Continued running 5 1/2' DP singles over 7/48 wireline from 780 m to 1090 m MD according to cut and thread procedure. Checked wireline and TDS top in coupling for wear every 25 joints." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1438m. The activity was categorized as 'interruption -- fish' and lasted for 4.2 hours. Operational details: Ran 5 1/2' DP singles over 7/48 wireline from 1090 m to 1438 m MD according to cut and thread procedure." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1438m. The activity was categorized as 'interruption -- fish' and lasted for 1.8 hours. Operational details: Laid out 5 1/2' DP singles on pipedeck. Measured and drifted joints. Moved weight bars on winch side of wiereline in order to move stress points. Checked rope socket - ok." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1438m. The activity was categorized as 'interruption -- fish' and lasted for 4.5 hours. Operational details: Laid out 5 1/2' singles on pipedeck. Cleaned and checked threads. Measured and drifted joints." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1438m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to continuing cut and thread operation." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1500m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Ran 5 1/2' singles over 7/48 wireline from 1438 m to 1500 m MD." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1500m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Wireline caught up behind AFT PRS arm. Removed wire and checked for damage - ok." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1640m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Continued running 5 1/2' singles over 7/48 wireline from 1500 m to 1640 m MD." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1640m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Cut back winch side of wireline. Re-built rope socket and fitted spearhead and new weights." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1750m. The activity was categorized as 'interruption -- fish' and lasted for 2.2 hours. Operational details: Continued running 5 1/2' singles over 7/48 wireline from 1640 m to 1750 m MD. Observed hydraulic leakage from TDS." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1750m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired hydraulic leakage on TDS." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1850m. The activity was categorized as 'interruption -- fish' and lasted for 2.8 hours. Operational details: Continued running 5 1/2' singles over 7/48 wireline from 1750 m to planned side entry sub depth of 1850 m MD." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1850m. The activity was categorized as 'interruption -- fish' and lasted for 1.2 hours. Operational details: Held toolbox talk for installing side entry sub. Assessed weather conditions and forecast. High winds > 40 knots and unfavorable forecast. Not able to perform riding belt operations required to re-position upper sheave wheel. Decided to continue running 5 1/2' DP singels over wireline to shoe depth." "On 2008-02-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1989m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Continued running 5 1/2' singles over 7/48 wireline from 1750 m to 1989 m MD." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2595m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: Ran 5 1/2' singles over 7/48 wireline from 1989 m to 2595 m MD. Winds 35- 40 knots." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Ran 5 1/2' singles over 7/48 wireline from 2595 m to 2704 m MD." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging TDS work platform." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Lowered and positioned TDS work platform." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Pulled wireline through TDS and secured same. Installed 5' weco blind plug in TDS top-in coupling." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Retracted and secured TDS work platform." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Performed derrick inspection due to period of high winds." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Pressure tested TDS 5' weco blind plug and K5 manifold valve 5/10 min 20/345 bar. Re-routed wireline over TDS." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Made up 4 m 5' pup joint to 5' x 5 1/2' x-over, threaded wireline through same." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Changed to 5' inserts in elevator. Picked up 5' pup/x-over and made up same to string." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2704m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removeing PS-30 automatic slips." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Removed PS-30 automatic slips, dressed same for 5' DP and re-installed in rotary. Ran in on 5' DP to 2707 m MD." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Took 9000 lbs tension on WL. Fitted T-bar to wireline and hung off on 5' DP." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 7.0 hours. Operational details: Fitted WL in sideentry sub. Cut WL and built rope sockets on winch and well ends according to Schlumberger procedure. Built WL torpedo. Changed from 5 1/2' to 5' saver sub on TDS." "On 2008-02-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather. Winds 60-70 knots. Meanwhile : -Inspected and greased PDM, HTS, IR, PS-21 and DP elevators -Inspected TDS torque wrench -Repaired trip tank pump -Installed drag chain guide on AFT PRS -Pressure tested standpipe and kill manifolds" "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.2 hours. Operational details: Waited on weather. Winds 50-60 knots. Meanwhile : -Installed drag chain guide on AFT PRS -Pressure tested standpipe and kill manifolds" "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Wind down to 45 knots. Performed derrick inspection after period of high winds. Assessed rigging alternatives for removal of upper sheave wheel in crown block." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing upper sheave wheel." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Barriered off drilfloor for aloft work. Brought rigging equipment to derrick. Rigged down upper sheave wheel." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 2.2 hours. Operational details: Rigged down WL sheave wheel from crown block. Lowered sheave wheel to drillfloor. Re-made torpedo due to tangeled wires in derrick. Powered up WL. Cleared and tidied drillfloor." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk for repositioning WL sheave." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Repositioned WL sheave in derrick. Attached wireline over sheave." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up side entry sub." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Made up side entry sub to toolstring according to Schlumberger instructions." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to testing IBOPs on TDS." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Rigged up swage with 1502 weco to TDS. Hooked up cement hose. Stopped for ESD test." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Halted operation for ongoing ESD test. Meanwhile : -Cleaned and tidied drillfloor and shaker areas -Changed die holders and dies on TDS torque wrench -Continued installation of dragchain guide on AFT PRS" "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Pressure tested upper/lower IBOP to 30/345 bar 5 /10 min. Meanwhile continued ESD testing." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Picked up stand of 5' DP and made up to side entry sub. Inserted rubber seals in side entry sub. Clamped 7/48 cable in side entry sub cut out." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2750m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: RIH with 5' DP from 2707 to 2750 m MD, held wireline tension contant at ~7000 lbs." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2750m. The activity was categorized as 'interruption -- fish' and lasted for 3.2 hours. Operational details: Broke circulation at 9 5/8' shoe and stepped up rate to 700 lpm as limited by erosion figures for side entry sub. Circulated bottoms up. Standpipe pressure rose from 10 bar to 30 bar throughout circulation. Mud weight out 1,39 sg rising to 1,43 sg towards the end. Mud weight in 1,45 sg. Gas peaked at 7% and levelled out on 0,3% towards end of circulation." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2750m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Held toolbox talk prior to running into open hole. Meanwhile flowchecked well and allowed well to equalize due to pipe/annulus imbalance." "On 2008-02-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2996m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: RIH with 5' DP from 2750 m to 2996 m MD, held wireline tension contant at ~7000 lbs. Made up TDS to each stand to limit backflow. At 2835 m MD, got indications on downhole tension that WL and fish were free, attempted to pull fish free with 12000 lbs WL tension - negative - WL still stuck." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3202m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: RIH with 5' DP from 2996 m to 3202 m MD, held wireline tension contant at ~7000 lbs. Made up TDS to each stand to limit backflow. Hole condtions good - no significant drag observed." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3202m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Broke circulation and cleaned grapple pumping 300 strokes at 1000 lpm. Observed imbalance pipe/annulus when stopped pumping - SPP 5 bar. Good corrspondance with downhole pressure of 430 bar read from log and 1,47 sg mudweight in annulus." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3202m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: RIH with 5' DP from 3202 m MD and caught fish at 3221 m MD. Set down ~5 MT on fish and observed indication of succesful catch on surface and downhole WL tension." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Picked up 10 m while allowing wireline to slack off - observed surface and downhole WL tension decreasing." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3167m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: Pulled 5' DP while feeding torpedo through upper and lower sheaves. Had to dismantle wire guides on lower sheave for torpedo to pass. Fitted T-bar and hung off wire in rotary. Slacked off wire and removed from depth counters on WL unit. Spooled torpedo onto WL drum and inserted WL back in depth counters." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2710m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: POOH wet with 5' DP from 3167 m to 2710 m MD. Maintained ~5000 lbs tension in wirieline while spooling in." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2710m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Flowchecked well - well static - ok. Removed snatch block from wireline." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2710m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Pumped 5 m3 1,65 sg slug at 700 lpm and chased to drillfloor." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2710m. The activity was categorized as 'interruption -- fish' and lasted for 1.2 hours. Operational details: Released electrical weakpoint. Powered down logging unit." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2710m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: POOH with WL inside 5 1/2' DP from 2710 m MD to surface." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Broke out side entry sub and laid down same. Cut loose WL from side entry sub. Rigged down lower sheave and secured upper sheave above V-door." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to changing handling equipment." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2707m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Changed slips segments. Re-activated guides in PS-30 automatic slips." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2703m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Broke out and and laid down 5' x 5 1/2' x-over with 5' pup joint." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.8 hours. Operational details: POOH with 5 1/2' DP from 2703 m MD to surface." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: Installed C-plate in rotary and hung off MDT toolstring. Broke off tool socket sitting in grapple. Parted and pulled toolstring sections using tugger. Broke off grapple and circulation sub and set back last stand of 5 1/2' DP." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up jet sub and BOP test plug." "On 2008-02-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 160m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Cleared and tidied drillfloor. Picked up and made up jet sub. RIH on 5' DP from surface to 160 m MD." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 160m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Washed accross subsea wellhead with jet sub 4 times pumping at 3000 lpm." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 300m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Made up test plug and RIH with same on 5' DP. Landed test plug in subsea wellhead/wearbushing at 140 m MD. Flushed lines from cement unit and verified line up." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 300m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: Tested 18 3/4' surface BOP against tests plug in subsea wellhead, 20/345 bar 5/10 min." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 300m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.0 hours. Operational details: Tested 18 3/4' surface BOP against test plug in subsea wellhead, 20/345 bar 5 /10 min. Meanwhile : -Serviced TDS -Removed 7/48 WL sheaves from derrick -Changed elevators -Cleaned and maintained drillfloor equipment" "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 160m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: POOH with 5 1/2' DP from 300 m to 160 m MD. Broke out and laid down test plug." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH with 5' DP from 160 m MD to surface. Broke out and laid down jet sub." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: Cleaned and tidied drillfloor prior to bringing in logging tools." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to running MDT toolstring." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 41m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: Ran MDT toolstring in sections to 41 m MD using C-plate and tugger according to Schlumberger instructions." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 41m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Changed dies in IR. Made up AH-3 1/2' x 4 1/2' IF x-over to 5' DP stand. Made up x-over to MDT logging string." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 41m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Connected locomotive to docking head. Schlumberger tetsed MDT toolstring. Disconnected locomotive." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 41m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to RIH with MDT toolstring on 5' DP." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 200m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: RIH with MDT toolstring on 5' DP from 41 m to 200 m MD. Max running speed 2 min/stand." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 200m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Removed master bushing and inserted PS-30 automatic slips in rotary." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 734m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.2 hours. Operational details: RIH with MDT toolstring on 5' DP from 200 m to 734 m MD. Max running speed 2 min/stand." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 734m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Broke circulation and brought pumps up to 1800 lpm for 5 mins." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 734m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Installed 5' x 5 1/2' x-over. Changed to 5 1/2' handling equipment." "On 2008-02-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2267m. The activity was categorized as 'formation evaluation -- log' and lasted for 5.0 hours. Operational details: RIH with MDT toolstring from 734 m to 2267 m MD on 5 1/2' DP. Max running speed 2 min/stand. Circulated 500 lpm / 3 mins every 500 m." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2751m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: RIH with MDT toolstring from 2267 m to 2751 m MD on 5 1/2' DP. Max running speed 2 min/stand. Circulated 500 lpm / 3 mins every 500 m." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Installed and made up 5 1/2' x 5' x-over and 5' pup joint for circulation." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.8 hours. Operational details: Circulated 2 x bottoms up pumping at 2000 lpm / SPP 93 bar. Gas peaked at 6,6% on 1st bottom up and levelled out on 0,2% after 2nd bottom up. MW in/out 1,44/1,44 sg. Tested rheology and found mud to be in good condition." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.8 hours. Operational details: Rigged upper and lower sheave wheels. Deactivated guides in PS-30 automatic slips. Lifted side entry sub with tugger and put locomotive into pipe. Spooled out approx 100 m on WL. Stabbed on side entry sub and lowered upper sheave wheel to centre position." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2759m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.0 hours. Operational details: Made up side entry sub. Made up 5' stand for pumping down locomotive. Pumped down locomotive while spooling out wireline. Pumpe rate 420-510 lpm / SPP 15-18 bar." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2759m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Increased pump rate to 1000 lpm / SPP 37 bar before latching locomotive in docking head. Observed 7 bar pressure increase when docking." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2759m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Powered up logging tools. Schlumberger tested MDT toolstring." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2759m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Clamped 7/46 cable in side entry cut out. Tested cable docking by applying 3500 lbs overpull on wireline for 5 mins - ok." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2759m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to RIH with MDT toolstring on 5' DP / 7/46 cable. Went through well control contingencies. Function tested hydraulic wireline cutter - ok." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3421m. The activity was categorized as 'formation evaluation -- log' and lasted for 8.8 hours. Operational details: RIH with 5' DP and 7/46 cable. Pumped 650 lpm when moving string downwards. Performed pressure point sampling in Hugin formation from 3252 m to 3412 m MD according to instructions from geologist. Hole condition good - no significant drag observed." "On 2008-02-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3418m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.8 hours. Operational details: Correlated and took station at 3417,5 for fluid sampling. Performed fluid sampling. Lined up to trip tank and monitored well continously while performing sampling." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3418m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: Performed fluid sampling at 3417,5 m MD. Obtained 2 ea 450 cc samples. Monitored well on trip tank." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3412m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: Pumped 6 m3 slug and allowed active to stabilize. Correlated and took station at 3412,5 m MD." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3412m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.8 hours. Operational details: Performed fluid sampling at 3412,5 m MD. Monitored well on trip tank. Observed downhole tool failure. Adequate sample not obtained from this station." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3412m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Troubleshot tool failure. Not able to function probe and pumps indicating problems with high voltage circuit. Checked surface equipment and confirmed ok. Discussed situation. Decided to start pulling out of hole." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3244m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Pulled logging tool free with ~5 MT overpull on block. Got overpull alarm 18 000 lbs on downhole tension. Communication with logging tools ok, but still unable to function high voltage circuit. POOH with 5' DP from 3412,5 m to 3244 m MD. Maintained 2500 lbs pull in wireline while pulling out." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2757m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: POOH with 5' DP from 3244 m to 2757 m MD. Hole in good condtion - no significant drag observed." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2757m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Removed clamps from side entry sub. Took overpull on wireline and released locomotive from docking head." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Broke out side entry sub and laid down locomotive." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Checked locomotive and cable - ok. Cut cable loose from side entry sub." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: Circulated bottoms up at 2000 lpm / 82-95 bar SPP. Gas peaked at 6,6% at bottoms up. MW in/out 1,45 sg." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Flow checked well - well static - ok." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Pumped 6 m3 1,62 sg slug and chased to drillfloor. Allowed active to stabilize." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2751m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Held toolbox talk. Changed inserts in PS-30 automaitic slips. Broke out and laid down 5' pup joint and 4 1/2' IF x 5 1/2' FH x-over." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2550m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH with MDT toolstring on 5 1/2' DP from 2751 m to 2550 m MD. Got problems with drawwork." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2550m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot problems with drawwork." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 734m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.0 hours. Operational details: POOH with MDT toolstring on 5 1/2' DP from 2550 m to 734 m MD." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 734m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: Changed handling equipment from 5 1/2' to 5'. Broke out and laid down 4 1/2' IF x 5 1/2' FH x-over." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 41m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.2 hours. Operational details: POOH with MDT toolstring on 5' DP from 334 m to 41 m MD." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: Parted and pulled MDT toolstring sections using C-plate and tugger. Found signs of short circuit in bulkhead coupling. Inner rubber packing on quicksilver probe was worn and torn." "On 2008-02-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Cleared and tidied drillfloor. Ran stand of 5' DP to help breaking off 5' saver sub." "On 2008-02-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.8 hours. Operational details: Changed from 5' to 5 1/2' saver sub in TDS. Changed die holders and dies in TDS torque wrench. Pulled 5' stand and racked back. Broke and laid down 5' pup, 5' x 5 1/2' x-over and AH-3 1/2' x 4 1/2' IF x-over. Meanwhile packed and disconnected MDT and WL containers for backload/removal." "On 2008-02-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.2 hours. Operational details: Cleared and tidied drillfloor. Brought casing running equipment to V-door. Removed PS-30 automatic slips. Installed Odfjell FMS in rotary. Positioned Odfjell casing tong on rails in front of IR. Prepared for rigging down WL sheave." "On 2008-02-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: RD WL sheave and installed HTS roller section. Drifted pipe on setback." "On 2008-02-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held tool box talk for RU to run 7' liner. Moved HTS rollers to aft end of cantiliver. Changed inserts in elevator and RU Odfjell csg tong." "On 2008-02-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Held tool box talk prior to running 7' liner. MU and RIH with shoe track and landing collar. Checked shoe and float collar for flow-through. Thread locked first 4 connections." "On 2008-02-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 289m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: RIH with 7' liner from 40 m to 289 m MD, filling every 5th joint. Max running speed was 5 joints/hr Installed pip-tag 0.34 m below top of collar on 1.92 m pup-joint in RA assembly. Estimated RA depth is 3216.17 m, but final depth will be given when 7' liner is set." "On 2008-02-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 734m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: RIH with 7' liner from 289 m to 734 m MD, filling every 5th joint. Max running speed was 9 joints/hr." "On 2008-02-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 842m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 7' liner from 734 m to 842 m MD, filling every 5th joint. Max running speed was 5 joints/hr. Filled liner completely before picking up hanger assembly." "On 2008-02-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 850m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Changed to 5½' DP elevators. P/U hanger/TSP packer assembly and MU same as per Weatherford procedure. Removed 7' FMS slips, installed master bushing. Filled PBR with Hi-visc mud. Took up/down weight 105/95 MT." "On 2008-02-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 850m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RD Odfjell csg tong. Removed HTS rollers. Cleared and cleaned rig floor." "On 2008-02-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 860m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PU 1 std of 5 1/2' HWDP. Changed to PS21 slips. RIH with 7' liner hanger on 5 1/2' HWDP from 850 m to 860 m MD." "On 2008-02-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 925m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 7' liner hanger on 5 1/2' HWDP from 860 m to 925 m MD." "On 2008-02-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 925m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Changed out 2 stds of 5 1/2' HWDP with 5 1/2' DP." "On 2008-02-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3392m. The activity was categorized as 'drilling -- casing' and lasted for 14.8 hours. Operational details: RIH with 7' liner from 925 m to 3392 m MD, filling every 5th stds. Max running speed was 8 stds/hr in cased hole and 5 stds/hr in open hole. Broke circulation at shoe at 2750 m, 1000 lpm / 53 bar." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3392m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Took 15 MT weight at 3392 m MD. MU TDS and attempted to work past tight spot with 20-30 MT. Up weight 181 MT / down weight 141 MT. Applied 9400 Nm RH torque when working string up. Released torque when working down." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3392m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke circulation, 230 lpm / 37 bar and established rate at 530 lpm / 49 bar. Washed down to tight spot applying max 20 MT. Observed pressure increasing to 60 bar. Shut down pumpe. Recorded 22 bar back pressure trapped below shoe. Applied 9400 Nm RH torque and worked string up. Recorded up weight of 151 MT, 30 MT upweight less than previous. Liner hanger RT most likely released from 7' liner." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3392m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Discussed further action and monitored well on trip tank." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3392m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Attempted to break circulation, negativ. Stopped pump at 45 bar after 243 ltrs pumped. Bleed off pressure to zero." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3392m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Discussed further action with town and monitored well on trip tank." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3399m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PU and established up weight at 151 MT. Slacked off weight at 130 MT and observed no drag. Unable to tag liner. Broke circulation 220 lpm / 22 bar which indicated that we were circulating through 5 1/2' DP and liner hanger RT. 7' liner most likely dropped further down." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3340m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with 7' liner hanger RT on 5 1/2' DP from 3399 m to 3340 m MD." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1520m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: POOH with 7' liner hanger RT on 5 1/2' DP from 3340 m to 1520 m MD." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1520m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Stopped POOH due to 65 knots wind. Installed TIW and monitored well on trip tank. Performed wind checks." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.2 hours. Operational details: POOH with 7' liner hanger RT on 5 1/2' DP from 1520 m to OOH. Inspected liner hanger RT. Found hydraulic release activated. All items intact on RT." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Cleared rig floor and serviced PS21 slips. Installed and function tested PS21 slips. Had approx. 30 min interruption in operation due to 65 knots wind." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 443m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: RIH with 20 std 5 1/2' DP 24.7 lbs/ft to 443 m." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 443m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Stopped RIH and had time-out due to sensor target bracket (570 g) dropped from TDS. Investigated and reported dropped object situation prior to re-commencing operations." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 806m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH with 20 std 5 1/2' DP 24.7 lbs/ft from 443 to 806 m." "On 2008-03-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 720m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: LO 5 1/2' DP 24.7 lbs/ft in singles from 806 m to 720 m." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 309m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: LO 5 1/2' DP 24.7 lbs/ft in singles from 720 m to 309 m." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: LO 5 1/2' DP 24.7 lbs/ft in singles from 309 m to OOH." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held time-out for safety with day crew. Inspected derrick in daylight due to yesterdays dropped object." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 444m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: RIH with 5 1/2' DP 24.7 lbs/ft to 444 m." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: LO 10 stds of 5 1/2' DP 24.7 lbs/ft in singles." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 5.2 hours. Operational details: Had tool box talk with drill crew. Performd cut and slip of drill line." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: Continued to LO stds of 5 1/2' DP 24.7 lbs/ft in singles." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed to 3 1/2' handling equipment and installed master bushings to be able to MU spear assembly. Found that pack-off on spear assembly was wrong size. Discussed further action." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed back to 5 1/2' handling equipment. Made arrangement with town to mobilize the correct size pack-off with helicopter." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued to LO stds of 5 1/2' DP 24.7 lbs/ft in singles." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed to 3 1/2' handling equipment and installed master bushings to be able to MU spear assembly." "On 2008-03-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk prior to picking up spear. MU spear assembly according to Weatherford's instructions." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued MU spear assembly according to Weatherford's instructions." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Re-arranged DP in derrick whilst waiting for new pack-off for spear assembly to arrive with helicopter." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Installed and MU new pack-off on spear assembly." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 693m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with spear assembly. Changed to 5 1/2' handling equipment and installed PS21 slips. RIH with spear assembly on 3 stands of 5 1/2' HWDP from 11 m to 129 m MD. RIH with spear assembly on 5 1/2' DP from 129 m to 693 m MD." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2466m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with spear assembly on 5 1/2' DP from 693 m to 2466 m MD. Meanwhile changed out csg tong on fwd iron roughneck." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2466m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Broke circulation at 2466 m and pumped 104 m3 1.45 sg mud at 2000 lpm / 88-94 bar. Continued to circulate due to gas peaks at 3.35%. Reduced circulation rate to 1000 lpm / 29,8 bar, when no gas in returns. Pumped at total of 175 m3. Meanwhile circulating, inspected PRS and dragchain. Found lock nuts loose and missing." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2466m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Repaired AFT PRS dragchain. RD equipment from repair and cleared rig floor. Meanwhile monitored well on trip tank." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with spear assembly on 5 1/2' DP from 2466 m to 2562 m MD while circulating 490 lpm / 18.4 bar. Upweight 152 MT / down weight 130 MT. Observed pressure increasing to 45 bar at 2562 m when sliding string into 7' liner. TOL = 2557 m MD. Stopped pumping and bled off pressure." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2563m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued to RIH 1.5 m and activated grapple with 3 left hand turns. First attempt to engage grapple failed, but the second attempt was sucessfull. Took 10 MT overpull. Established circulation at 265 lpm / 32 bar. PU to 191 MT (10 MT above liner weight) and circulated for 15 min. PU to 226 MT (45 MT overpull) and observed 7' liner break free." "On 2008-03-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3122m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Changed bit depth to include 7' liner. Pumped OOH 265 lpm / 32 bar with 7' liner on 5 1/2' DP from 3414 m to 3122 m MD." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Pumped OOH 265 lpm / 32 bar with 7' liner on 5 1/2' DP from 3122 m to 2755 m MD." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2755m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Circulated btms up at csg shoe to clear passage around 7' liner and liner hanger, 1000 lpm / 59 bar. Continued to circulate due to gas peaks at 6.8%. Pumped at total of 113 m3. Flow checked well prior to POOH." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2716m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped slug and POOH with 7' liner on 5 1/2' DP from 2755 m to 2716 m MD." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 867m. The activity was categorized as 'drilling -- casing' and lasted for 8.8 hours. Operational details: POOH with 7' liner on spear assembly from 2716 m to 867 m MD. Spaced out inside BOP. Flow checked for 15 min on last joint of 5 1/2' DP. Changed out PS21 with master bushing before POOH with 2 stds of 5 1/2' HWDP." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 852m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: LO bumper sub. Held pre-job meeting and SJA. Released spear and LO same." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 852m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held tool box talk with involved personnel. RU Odfjell csg tong with low marking dies and csg handling equipment." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 844m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: LO liner hanger." "On 2008-03-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 560m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: POOH with 7' liner and RB in derrick from 844 m to 560 m MD." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: POOH with 7' liner and RB in derrick from 560 m to OOH." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RD Odfjell csg tong and csg handling equipment." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RD Odfjell csg tong and csg handling equipment." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 75m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: PU and MU 8 1/2' wiper trip BHA." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1010m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5' DP from 75 m to 1010 m MD. Held time-out for safety due to dropped pin from fwd PRS dragchain. Highlighted 'red zone' policy." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1010m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: MU TDS and tested MWD, 2000 lpm / 146 bar. Changed mud pumps and stand pipes to optimize signal from MWD." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1501m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5' DP from 1010 m to 1501 m MD." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1501m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held time-out for safety due to dropped pin from fwd PRS dragchain. Highlighted 'red zone' policy." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1501m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Inspected aft PRS dies. Moved 5 1/2' HWDP from finger board. Installed totco ring in 5' DP. Changed to 5 1/2' handling equipment and installed X-over." "On 2008-03-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2146m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5 1/2' DP from 1501 m to 2146 m MD. Filled pipe every 10 stds." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2751m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5 1/2' DP from 2146 m to 2751 m MD. Filled pipe every 10 stds." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2751m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: MU TDS and filled pipe and broke circulation at 9 5/8' csg shoe with 500 lpm / 21 bar. Up weight 149 MT / down weight 122 MT. Circulated btms up at 2000 lpm / 164 bar. Max gas 2.2%. ECD = 1.58 sg." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3320m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5 1/2' DP from 2751 m to 3320 m MD. Filled pipe every 10 stds." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5 1/2' DP from 3320 m to 3395 m MD. Worked pipe to pass tight spot at 3395 m. MU TDS and rotated pipe 1/2 turn. Worked past tight spot and continued RIH to 3420 m." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3478m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5 1/2' DP from 3420 m to 3478 m MD. Worked pipe to pass tight spot. MU TDS and applied 30 rpm and pumped 500 lpm / 38 bar. Worked past tight spot and reamed up to 3420 m. Came down from 3420 m to 3478 m with no rotation and no flow." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3510m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Washed down with 8 1/2' wiper trip BHA on 5 1/2' DP from 3478 m to 3510 m MD, 1400 lpm / 128 bar, 50 rpm / 13-14 kNm." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3510m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Circulated 3 x btms up and conditioned mud at 3510 m whilst rotating and reciprocating string. Increased flow in steps up to 2200 lpm / 206 bar, 150 rpm / 13-17 kNm to be able to control ECD. Max MW out of hole 1.56 sg. Final ECD 1.57 sg. Max gas 9.3%." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3387m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: RB 1 std from 3510 m to 3478 m. No obstruction encountered. Worked 1 std from 3478 m to 3437 m, 2200 lpm / 201 bar, 150 rpm / 12-15 kNm. RB and reamed 1 std from 3437 m to 3397 m. Observed tight spots at 3428 m and 3423 m. Reamed through tigh spots with reduced flow of 1500 lpm due to packing off. Staged up parameteres to 2200 lpm / 200 bar while working through tight spots. RB 1 std and circulated btms up whilst rotation and reciprocating pipe from 3397 m to 3357 m, 2200 lpm / 198 bar, 100 rpm / 12-14 kNm." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3510m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' wiper trip BHA on 5 1/2' DP from 3387 m to 3508 m MD. No obstruction encountered. Observed 1.5 m fill at TD." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3510m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Circulated btms up at 3510 m, 2200 lpm / 196 bar, 100 rpm / 12-14 kNm. Up weight 178 MT / down weight 134 MT. Readings to give comparison for liner running: Rotating 10 rpm / 11-12 kNm, 15 rpm / 11-13 kNm, 20 rpm / 10-13 kNm. Rotating upweight 172 MT / rotating down weight 137 MT. Pumping 500 lpm / 19 bar, 1000 lpm / 54 bar, 1500 lpm / 102 bar. Distance from neutral to up weight is 0.6 m." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flow checked well. Static." "On 2008-03-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3114m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: POOH with 8 1/2' wiper trip BHA on 5 1/2' DP from 3508 m to 3271 m MD wet. No obstruction encountered. Pumped slug. Continued to POOH from 3271 m to 3114 m MD. Pulled through tight spot at 3237 m with 25 MT overpull. Worked pipe several times to pass tight spot." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2748m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' wiper trip BHA on 5 1/2' DP from 3114 m to 2748 m MD." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2748m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flow checked well inside shoe. Static. Dropped 2 3/4' rabbit." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: POOH with 8 1/2' wiper trip BHA on 5 1/2' DP from 2748 m to 1500 m MD. Torque reading at 7' liner hanger setting depth: 10 rpm / 6-8 kNm, 15 rpm / 6-9 kNm, 20 rpm / 6-9 kNm. At 7' liner hanger setting depth; up weight 147 MT / down weight 125 MT." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed to 5' handling equipment." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 928m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' wiper trip BHA on 5' DP from 1500 m to 928 m MD." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 74m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with 8 1/2' wiper trip BHA on 5' DP from 928 m to 74 m MD." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 74m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flow checked well prior to pulling BHA through BOP. Meanwhile held tool box meeting prior to BHA handling." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 74m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed net around fwd PRS for prevention of dropped objects." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: POOH with 8 1/2' wiper trip BHA on 5' DP from 74 m to 46 m MD. Removed PS21 slips and installed master bushings. LO 8 1/2' wiper trip BHA from 46 m to OOH. Cleaned and cleared rig floor of excess equipment." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Held tool box talk for RU to run 7' liner. Installed HTS rollers. Changed inserts in elevator and RU Odfjell csg tong." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Inspected PRS and TDS for loose items. Greased PRS and TDS." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 39m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held tool box talk prior to running 7' liner. MU and RIH with shoe track and landing collar. Checked shoe and float collar for flow-through." "On 2008-03-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 434m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 7' liner from 39 m to 434 m MD, filling every 5th joint. Cleaned and re-doped pin end. Max running speed was 9 joints/hr Installed pip-tag 0.34 m below top of collar on 2.05 m pup-joint in RA assembly. Estimated RA depth is 3230.76 m, but final depth will be given when 7' liner is set." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 812m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 7' liner from 434 m to 812 m MD, filling every 5th joint. Cleaned and re-doped pin end. Max running speed was 6 joints/hr. LO joint #139 and changed out box on joint #140. Replaced joint #139 with joint #115." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 835m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 7' liner from 434 m to 812 m MD, filling every 5th joint. Cleaned and re-doped pin end. Filled liner completely before picking up hanger assembly." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 850m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Changed to 5½' DP elevators. P/U hanger/TSP packer assembly and MU same as per Weatherford procedure. Removed 7' FMS slips, installed master bushing. Filled PBR with drillwater and checked shear pins. Took up/down weight 105/95 MT." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 850m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RD Odfjell csg tong. Removed HTS rollers. BO XO on HWDP and drifted same. Cleared and cleaned rig floor." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 963m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: PU 1 std of 5 1/2' HWDP. Changed to PS21 slips. RIH with 7' liner hanger on 5 1/2' HWDP from 850 m to 963 m MD." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3392m. The activity was categorized as 'drilling -- casing' and lasted for 9.0 hours. Operational details: RIH with 7' liner from 963 m to 3392 m MD, filling every 5th stds. Broke circulation at shoe at 2756 m for 5 min, 500 lpm / 17 bar. Worked past tight spot at 3358 and turned pipe 1/2 turn. Max running speed was 10 stds/hr in cased hole and 6 stds/hr in open hole." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3510m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 7' liner from 3392 m to 3468 m MD, filling every 5th stds. MU last std and broke circulation. Staged up pumps to 340 lpm / 23 bar and washed down. Tagged TD at 3510 m MD. Up weight 190 MT / down weight 142 MT." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Installed and MU cmt head. Spaced out liner to 3508 m / top liner hanger at 2665,6 m." "On 2008-03-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Established circulation and increased pump rate in steps to 1140 lpm / 78 bar. Circulated 1 1/2 open hole volume (45 m3). Meanwhile pressure tested cmt line to 345 bar." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continued to circulate 1 1/2 open hole volume, 1140 lpm / 78 bar." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Reduced pump rate to 200 lpm. Dropped the ball from the cmt head with liner in tension and chased the ball with 500 lpm / 30.6 bar. Landed ball after 653 stks pumped. Pressured up to 135 bar. Held 2 min. Bled down to 70 bar. Sat down 25 MT of drill pipe weight to verify that hanger was set. OK. Continued to pressure up to 175 bar to relese setting tool. Held 1 min. Continued to pressure up to shear out ball seat. Sheared at 228 bar. PU to verify that liner was released. Up weight 158 MT / down weight 134 MT." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Sat down weight to 130 MT. Established circulation while rotating and increased pump rate in steps up to 1200 lpm / 74 bar, 20 rpm / 10-12 kNm. Pumped 95 m3. Meanwhile held pre-job meeting for cmt job." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Pumped 10 m3 base oil, 780 lpm / 80 bar and 15 m3 of 1.65 sg tuned spacer E+ at 665 lpm / 80 bar with mud pumps while rotating liner 15 rpm / 12 kNm. Lined up to cmt unit through cmt hose. Dropped dart to release bottom wiper plug. Mixed and pumped 15.9 m3 1.90 sg cement slurry at 680 lpm / 80 bar and displaced cement with 0.9 m3 freshwater to rig floor. Dropped dart to release top wiper plug. Lined up to rig pumps and pumped 19 stks before flag indicated dart had dropped. Displaced cement with 45 m3 OBM at 1200 lpm, 15 rpm / 15-18 kNm with full returns. Slowed down pump rate to 500 lpm after 1930 strks. FCP = 42 bar. Stopped pumping after 2052 + 19 = 2071 strks pumped. Observed torque increased to 26 kNm after 2071 strks pumped, but had no bump." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Checked for back flow. Ok. RD cmt hose." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Sat TSP packer according to Weatherford procedure. Closed annular and pressured up to 300 bar. Pressure tested TSP packer to 300 bar / 10 min with 1.45 sg OBM." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Released liner hanger RT by pressuring up to 70 bar. Pulled and measured RT out of PBR. Increased rate to 1000 lpm when pressure dropped. Dropped 2 sponge balls and circulated DP clean. Circulated out excess cmt, 2000 lpm / 80 bar. Observed cmt and spacer in returns. Circulation pressure increased to 98 bar and then level out." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: LO cmt head and 10 ft pup joint." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 112m. The activity was categorized as 'drilling -- casing' and lasted for 8.5 hours. Operational details: POOH with 7' liner hanger RT on 5 1/2' DP from 2667 m to 112 m MD. RU rollers on HTS and cleared rig floor of excess equipment prior to LO pipe in singles. LO 13 stds of 5 1/2' DP 24.7 lbs/ft in singles. Pumped 3 m3 1.63 sg slug, 1000 lpm / 7 bar at 594 m." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with 7' liner hanger RT on HWDP from 112 m to OOH. Removed PS21 auto slips and installed manual slips. Disconnected HTS back rollers. BO and LD 7' liner hanger RT. Found both wiper plugs attached to liner hanger RT and both darts and one sponge ball inside RT." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Changed to 3 1/2' handling equipment. PU 3 1/2' fishing assembly. Broke connections and LO Mærsk pup joint and XO. Cleaned and cleared rig floor." "On 2008-03-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RU 7' csg tong and handling equipment. Inspected PRS dies and rollers." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PU 7' liner shoe track std and attempted to break baker locked connections. Unsucessful. RB in derrick." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 738m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: RIH with 7' liner stds from derrick to 738 m MD. Removed grub screws from top-most centralizer/stop collar on each std." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 671m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Installed HTS back rollers. POOH and LO 7' liner in singles from 738 m to 671 m MD." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: POOH and LO 7' liner in singles from 671 m to OOH." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: PU 7' liner shoe track std and attempted to break baker locked connections with csg tong without sucess." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RD csg tong and 7' liner handling equipment. Meanwhile performed csg test. Observed pressure rise to 290 bar before dropping, 2426 ltrs pumped and 1600 ltrs returned." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: PU 7' liner shoe track std and broke baker locked connections using manual tongs. Cleaned and cleared rig floor and changed to 5 1/2' handling equipment." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: PU and MU jet sub assembly. RIH and washed BOP cavity. Staged up pumps to 3125 lpm / 43 bar and washed through cavity several times." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 184m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Made up test plug and inspected seals. RIH with same on 5 1/2' DP. Landed test plug in subsea wellhead/wearbushing at 140 m MD. Flushed lines from cement unit and verified line up." "On 2008-03-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 184m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: Tested 18 3/4' surface BOP against test plug in subsea wellhead, 20/345 bar 5/10 min." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 184m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.5 hours. Operational details: Tested 18 3/4' surface BOP against test plug in subsea wellhead, 20/345 bar 5/10 min. Meanwhile performed derrick inspection, cleaned moonpool area and prepared for greasing manifolds." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with jet sub/BOP test plug on 5 1/2' DP from 184 m to 165 m MD." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH with jet sub/BOP test plug on 5 1/2' DP from 165 m to OOH. Broke out and LD test plug." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: RU 3 1/2' handling equipment. MU kelly cock and grey valve assembly for testing." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 4.5 hours. Operational details: Tested 3 1/2' kelly cock and grey valve. Tested kill and standpipe manifolds. Tested 5 1/2' kelly cock and grey valve. Meanwhile changed out drill line spooler." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Took time-out for safety due to dropped bulldog clamps from drill line." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Continued to change out drill line spooler." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 13m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Held tool box meeting with involved personnel. MU and RIH with 6' PDC bit and scraper assembly from surface to 13 m." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 13m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Repaired damaged fittings on HTS rollers." "On 2008-03-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 550m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: RIH with 6' PDC bit and scraper assembly from 13 m to 26 m. Changed to PS21 slips. Continued to RIH with 6' PDC bit and scraper assembly on 3 1/2' DP from 26 m to 550 m. PU 3 1/2' DP in singles. Max running speed was 14 joints/hr. Meanwhile tested choke manifolds." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 804m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RIH with 6' PDC bit and scraper assembly on 3 1/2' DP from 550 m to 804 m. Max running speed was 13 joints/hr." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 804m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Changed from 3 1/2' handling equipment to 5 1/2' handling equipment." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1977m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: RIH with 6' PDC bit and scraper assembly on 5 1/2' DP from 804 m to 1977 m." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2650m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RIH with 6' PDC bit and scraper assembly on 5 1/2' DP from 1977 m to 2650 m." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2650m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Broke circulation with rotation and circulated btms up, 1824 lpm / 290 bar, 20 rpm / 7 kNm. Up weight 141 MT / down weight 122 MT / rotating weight 130 MT." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3430m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Entered 7' liner PBR with reduced flow, 400 lpm / 45 bar. Observed no drag. Continued RIH with 6' PDC bit and scraper assembly on 5 1/2' DP from 2650 m to 3430 m." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3430m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: MU TDS and washed down with scraper string from 3430 m to 3460 m, 1110 lpm / 143 bar. Up weight 159 MT. Pulled back and scraped liner interval 3440-3450 m, 1790 lpm / 300 bar, 60 rpm / 10 kNM. Circulated 1 1/2' btms up at 1790 lpm / 300 bar. RB one std and flow checked well static. Ok." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3228m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 6' PDC bit and scraper assembly on 5 stds of 5 1/2' DP wet from 3430 m to 3228 m. Flow checked well static. Ok." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 807m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Pumped slug and continued to POOH with 6' PDC bit and scraper assembly on 5 1/2' DP from 3228 m to 807 m." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 807m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Changed from 5 1/2' handling equipment to 3 1/2' handling equipment. Serviced foldable fingerboard. Meanwhile flow checked well static. Ok." "On 2008-03-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 685m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 6' PDC bit and scraper assembly on 3 1/2' DP from 807 m to 685 m." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 578m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: POOH with 6' PDC bit and scraper assembly on 3 1/2' DP from 685 m to 578 m." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 578m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Observed yellow UFO flying/falling from derrick and out side/aft of derrick. Inspected PRS, derrick and drillfloor, but were not able to man-ride due to 50 knots wind. Nothing out of the ordinary was found." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 57m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH with 6' PDC bit and scraper assembly on 3 1/2' DP from 578 m to 57 m." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 57m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Retrieved 3 1/2' DP std that was pulled out of fingerboard by PRS lower arm due to human error. Held time-out for safety. Prepared equipment to be used for retrieving std. Instected fingerboard. RB 3 1/2' DP std in fingerboard." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 6' PDC bit and scraper assembly on 3 1/2' DP from 57 m to OOH. LD 6' PDC bit and scraper assemblies." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk prior to make up and RIH with EZSV plug and Circ. Sub. Made up EZSV plug and Circ. Sub." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with EZSV plug and Circ. Sub to 42 m." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held tool box talk with day shift prior to change to PS -21 slips and RIH with EZSV plug and Circ. Sub on 3½' DP." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Changed to PS -21 slips and functioned same." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 792m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Continued RIH with EZSV plug and Circ. Sub on 3½' DP from 42m to 792m at 2 min/std." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 792m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Held tool box talk and changed over to 5½' surface handling equipment." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3448m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: Continued RIH with EZSV plug and Circ. Sub on 5½' DP from 792m to 2625m at 2 min/std. Reduced RIH speed as entering the 7' line at 2661m, continue to RIH to 3448m EZSV plug setting depth." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3448m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Took up/down weight 168/136 MT. Established circulation at 220 lpm 12 bars. Reciprocated the string, increased rate in stages to 670 lpm 53 bars. Stopped circulation and positioned EZSV plug at setting depth at 3448m up stroke. Installed the EZSV plug as per Halliburton procedure. Picked up 20 MT to shear the tension sleeve. Set down 10 MT on EZSV plug. Picked up to 3440m." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held tool box talk prior to R/U for pressure testing of the EZSV plug and the 7' liner." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Rigged up surface lines, flushed lines and tested same to 300 bars 5 min. Closed upper pipe rams and tested the EZSV plug and 7' liner to 300 bars 10 min. 2023 litres pumped and same in return." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Rigged down surface test lines." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3440m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Flow checked prior to POOH with the EZSV plug RT and the circ sub." "On 2008-03-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3252m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH wet with 5 std to 3252m." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 791m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Pumped slug of 5.5m³ 1.66 SG. Continued POOH with 5½' DP and EZSV RT from 3252m to 791m." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 791m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held tool box talk prior to change over to 3½' surface handling equipment. Performed same." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 525m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued POOH with 3½' DP EZSV RT from 791m to 525m" "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH with 3½' DP and EZSV plug RT to surface." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Changed out PS -21 slips to master bushing. L/O EZSV plug RT." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH with BOP/riser clean out assy." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 314m. The activity was categorized as 'drilling -- other' and lasted for 3.8 hours. Operational details: Functioned shear rams. Picked up clean out assy and RIH and cleaned BOP, riser and WH. Function tested BOP rams and annular." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: POOH with clean out assy and laid out same." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Cleaned and cleared rig floor. Inspected aft PRS. Performed daily derrick inspection. Simultaneously prepared mule shoe for 7' line clean out assy." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 32m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Held tool box talk and broke out 6' bit and bit sub and made up 3½' mule shoe. Made up Razor Back assy. Installed PS-21 slips." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 776m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: RIH with 3½' mule shoe and Razor Back assy. From 32m to 776m." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 776m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Held tool box talk and picked up Weaterford PBR polish mill." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 778m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held tool box talk prior to install the 9 5/8' clean out assy." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 831m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Changed to 5½' DP handling equipment. Installed the 9 5/8' clean out assy." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 831m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up to TDS and broke circulation with 1000 lpm 72 bars. Installed PS-21 slips. Observed hydraulic leak in Aft PRS." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 831m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Repaired hydraulic leak on Aft PRS." "On 2008-03-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: Continued RIH with clean out assy. from 831m to 2080m" "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2646m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Continued RIH with clean out assy. from 2080m to 2646m." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2646m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated 50m³ OBM at 2100 lpm 295 bars. Took up/down weight zero/20 rpm. 144/123 MT - 137/129 MT." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2848m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Entered the 7' liner. Continued RIH with clean out assy. from 2646m to 2848m" "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2848m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up the 10 3/4' casing scraper assy." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3380m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Continued RIH with clean out assy. from 2857m to 3380m" "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Commenced to wash down from 3380m to 3420m. 40 rpm, 1000 lpm, 110 bars." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3445m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Continued RIH washing down from 3420m, tagged the PBR 1,5 m deep (at 2662,3 m) with 2 MT, with mule shoe at 3445m, and polished at 500 lpm, 40 bars and 13 kNm." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3435m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.2 hours. Operational details: Scraped 7'/9 5/8'/10 3/4' casing, dressed/polished 7' liner top. Pulled back to 3435m, increased pump rate to 1960 lpm, 292 bars and conditioned mud." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3445m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Set the Well Commissioner as per SPS instruction. Up/down weight with out pumping 167/137 MT, RIH and set down 13 MT on PBR. Closed upper pipe rams and pressured up the Well Commissioner in steps to 70 bars and monitored. Simultaneously held tool box talk prior to perform inflow test of the 7' liner and liner lap. Opened BOP. PU, relaxed well commisioner element." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3445m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Displaced choke & kill line to Base oil, then soap mix to fill lines." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3445m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Pumped 26 m³ Base oil + STP volume with 320 lpm, final pump pressure 147 bars (first 5m³ pumped at ~1000 lpm to clean lines). Final static pressure equaled = 134 bars, monitored same for 30 min. Re-set packer with 13.5 MT. New up/down weight 153/125 MT. Lined up to cement unit and equalised pressure across IBOP." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3445m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Bled down the drill pipe pressure in stages to 10 bars prior to performing inflow test. 680 liters bled back. Inflow tested the 7' liner and liner lap." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3445m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pressured up DP to 138 bars with cement unit to equalize pressure across the Well Commissioner, 633 litres pumped." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3444m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Picked up 150 MT and let Well Commissioner relax. Picked up 6m. Equalized CMT unit and bled down CMT lines. Ran back in to 3444m." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3444m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied trip tank." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3444m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Held tool box talk prior to pumping the washing train." "On 2008-03-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3444m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.2 hours. Operational details: Pumped washing train as per Halliburton program: 10 m3 dope cleaner pill, 30 m3 hivis push pill, 15 m3 hivis soap pill, 10 m3 seawater, 15 m3 hivis soap pill, 3200 lpm, 300 bars. Chased wash train with 209m³ of completion fluid, 2200 lpm, 155 bars. Checked packer fluid after displacement: < 0.01% solids." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3444m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.5 hours. Operational details: Cleaned all surface lines, kill-, choke-line and manifold. Circulated well and checked packer fluid for solids, only trace of solids." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Racked back one std in derrick. Held tool box talk prior to pressure testing the 7' liner/liner lap." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Lined up to the trip tank observed unstable gain. Closed in the well, investigated instability. No pressure built up. Checked the trip tank equipment, found that foaming was the reason." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Performed manually flow check of the well, static." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made CMT hose and leak tested same to 345 bars for 5min. Commenced pressure test of well to 345 bars." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pressure tested the well to 345 bars 10 min. Pumped 2.2m³ - return 2.2m³. Rigged down surface equipment." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Installed TIW valve & flow checked well. Added de-foamer to trip tank." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held tool box talk prior to slip and cut of drill line." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Commenced to slip and cut drill line. Found threads in deadman anchor block damaged. Simultaneously monitored well over the trip tank." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'interruption -- maintain' and lasted for 4.5 hours. Operational details: Re-cut the threads in the deadman anchor block. Simultaneously installed the Fairings on F-12 for the PR TBC using the ROV." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Disconnected the hang of line & re-calibrated the main block/TDS. Functioned Crown-O-matic, set at 54.4 m. Simultaneously installed the Fairings on F-7 for the PR TBC using the ROV." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2846m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Held tool box and changed to PS-21 slips. POOH from 3420m to 2846m." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2840m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Laid out the Razor back BHA # 3." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 770m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.2 hours. Operational details: Continued POOH with 5½' DP and wash string, from 2840m to 770m." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 760m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Laid out the Razor back BHA #2." "On 2008-03-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 735m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Changed to 3½' handling equipment. Picked up one std of 3½' from the derrick, continued POOH with 3½' DP and laid out in singles from 770m to 735m." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 475m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.5 hours. Operational details: Continued POOH with 3½' DP and laid out in singles from 735m to 475m." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 475m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: Stopped POOH due to exhaust from the production turbine blowing into the rig floor. Installed safety valve on to the 3½' DP. Monitored well on the trip tank." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 474m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Continued waiting due to exhaust fumes blowing into the rig floor." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.0 hours. Operational details: Held tool box talk and continued POOH with 3½' DP and washing string. Laid out 3½' DP in singles." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Commenced to rig up 5½' DP handling equipment, found that the Razor back could not fit into the basket. Rigged back up the 3½' handling equipment." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- wait' and lasted for 4.5 hours. Operational details: Shut down operation due to exhaust fumes blowing into the rig floor. Meanwhile held tool box talk prior to installation of the GTV plug. Meanwhile continued making up the flow line at WH for F-7. Prepared for nippling of BOP." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Broke out the Razor back assy and laid out same." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Changed to 5½' handling equipment and picked up the GTV RT/GTV plug." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Prepared for RIH with the GTV plug on 5½' HWDP." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.2 hours. Operational details: Shut down operation due to exhaust fumes blowing into the rig floor." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 44m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: RIH with the GTV plug on 5½' HWDP from surface to 44m." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 44m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Shut down operation due to exhaust fumes blowing into the rig floor." "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 564m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.2 hours. Operational details: RIH with the GTV plug on 5½' HWDP from 44m to 564m" "On 2008-03-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 564m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Shut down operation due to exhaust fumes blowing into the rig floor." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 564m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: Shut down operation due to exhaust fumes blowing into the rig floor." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 616m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: RIH with the GTV plug on 5½' HWDP/DP from 564m to 616m." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 616m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Broke out one double and made up TIW, pump in sub and 3m 5½' DP pup. Made up to TDS." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 616m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Took up/down weight 98/91 MT. Set GTV plug at per Baker procedure. Bottom of the plug at 617m mid. element 614.5m, slips 615m and top of plug at 612m." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 617m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: Made 2' 1502 chiksan, flushed lines. Attempted to leak test line, found to much air in the system. Filled up system and leak tested line to TIW and IBOP 380 bars 5 min." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 617m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Pressure tested the GTV plug from below to 380 bars 10 min., volume pumped 1.75m³ - 1.73m³ in return." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 617m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Rigged down surface lines TIW, pump in sub and 5½' DP pup. Disengaged running tool from plug." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 610m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Spotted 10m³ of hi-vis on top of GTV plug." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Held tool box talk prior to break/lay out the GTV RT." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Inspected the aft PRS's dies. POOH with the GTV RT from 612m to above the BOP." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Held tool box talk and closed the shear rams and pressure tested the GTV plug from above to 345 bars 10 min., volume pumped 830 litres - return 830 litres." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Laid out the GTV RT." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Cleaned and cleared the rig floor." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk and picked the wear bushing RRT. M/U on 5½' RIH and engaged the wear bushing at 139m took 60 MT over pull to free the wear bushing." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with the wear bushing. Laid out wear bushing and RRT. Found metal chip on the wear bushing." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up WH jetting sub." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Operation suspended due to exhaust fumes blowing into the rig floor." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with the WH jetting sub from surface to 129m. Discussed forward plan with town." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.8 hours. Operational details: Operation suspended due to exhaust fumes blowing into the rig floor." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued RIH to 138m and washed WH area with 5 rpm 2650 lpm 17 bars. POOH and laid out jetting sub." "On 2008-03-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Operation suspended due to exhaust fumes blowing into the rig floor. Meanwhile cleaned the moon pool, pit room and pump room." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Operation suspended due to exhaust fumes blowing into the rig floor. Meanwhile cleaned the moon pool, pit room and pump room." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 9.8 hours. Operational details: Operation suspended due to exhaust fumes blowing into the rig floor. Meanwhile cleaned the moon pool, pit room, pump room and general maintenance." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk and picked/made up the 10 3/4' Lock down sub." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 130m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH with the 10 3/4' Lock down sub to 130 m took up/down weight 78/74 MT." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed the 10 3/4' Lock down sub at 139.27m, as per Vetco procedure." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed line test from CMT unit to the rig floor to 207 bars 5 min." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pressure up to 207 bars 5 min to fully set of the 10 3/4' Lock down sub. Volume pumped 275 litres - 250 litres in return." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Released the 10 3/4'Lock down sub RT." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: POOH with the 10 3/4' Lock down sub RT and laid out same." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.8 hours. Operational details: WOW. Meanwhile inspected and serviced the aft PRS." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW. Held time out due to LTA on main deck." "On 2008-03-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: WOW. Continued servicing the aft PRS." "On 2008-03-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: WOW. Serviced and inspected the TDS." "On 2008-03-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW. Changed out the wash pipe." "On 2008-03-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW. Cleaned and cleared the rig floor" "On 2008-03-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: WOW. Cleaned and cleared the rig floor." "On 2008-03-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 11.8 hours. Operational details: WOW. Performed general maintenance. Cleaned kill manifold. Had derrick inspection. Serviced Carrier rollers, spinner and tracks on aft Roughneck." "On 2008-03-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW. Cleaned rig floor. Cleaned pit # 7. Performed maintenance on the aft PRS and the TDS." "On 2008-03-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WOW. Greased the UPR track on the PRS beam. Functioned main flow line valve 1250 psi. Transported 6 flood light to the finger board level in the derrick." "On 2008-03-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 13.0 hours. Operational details: WOW prior to retrieve the HP drilling riser. Meanwhile cleaned stand pipe/Choke line manifold. Changed oil on the TDS. Performed general maintenance and PM's. Changed out the cathead wire." "On 2008-03-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW prior to retrieve the HP drilling riser. Meanwhile prepared tools and lifting equipment, for nippling down the Diverter,BOP and the HPDR. Commenced installation of flood light in derrick. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 22:00 41/47 30° 6.1/9.7 360° 23:00 42/47 30° 6.2/9.8 10° 00:00 43/48 30° 6.1/9.7 360°" "On 2008-03-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WOW prior to retrieve the HP drilling riser. Continued installation of flood light in derrick. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 00:30 40/45 30° 6.4/10.1 360° 02:00 42/47 30° 6.1/9.6 10° 03:00 39/43 30° 6.0/9.6 10° 04:30 37/41 20° 5.6/8.8 360° 05:00 35/41 30° 5.3/8.4 10° 06:00 34/38 20° 4.9/7.9 10°" "On 2008-03-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 13.0 hours. Operational details: WOW prior to retrieve the HP riser. Meanwhile installed flood light in derrick. Commenced changing out the seal assy of BOP door. Cleaned pit # 9 & 11. Performed general maintenance and PM's. Moved CTS funnel from F-9 to F-1. Installed cover in CTS funnel. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 07:00 24/30 30° 4.4/10 10° 09:00 18/26 28° 4/10.4 30° 11:00 14/20 24° 3.7/7.8 40° 13:00 9/15 7° 3/9.4 340° 15:00 15/21 300° 2.8/9.8 225° 17:00 20/23 315° 2.9/8.9 250° 19:00 19/22 320° 2.6/4.1 340°" "On 2008-03-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW prior to retrieve the HP riser. Installed flood light in derrick. Cleaned pit # 6,8 & 10. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 21:00 18/22 320° 2.6/4.2 320° 23:00 20/23 340° 2.5/4 340°" "On 2008-03-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WOW prior to retrieve the HP riser. Completed installation of the flood light in the derrick. House keeping in the moon pool. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 01:00 7/9 360° 2.7/3.9 340° 03:00 11/15 340° 2.4/4.1 340° 05:00 15/18 350° 2.7/4.3 340° 07:00 12/14 350° 2.9/4.6 340°" "On 2008-03-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 13.0 hours. Operational details: WOW prior to retrieve the HP riser. Changed out of BOP door seal assy, greased manual valves on choke/kill line. Cleaned pit. Performed general maintenance and PM's. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 08:00 17/23 330° 2.6/4.1 350° 10:00 2.3/3.6 12:00 1.6/2.6 14:00 1.3/2.1 16:00 21/24 350° 1.8/2.9 330° 18:00 23/26 340° 3.1/5.0 340° 14:30-19:00 Not able to work at rig floor, due to exhaust fumes." "On 2008-03-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Performed general maintenance and PM's. Greased valves on BOP. Disconnected the CRI hose from F-12 and removed the check valve. Connected up the CRI hose again and opened to annulus, annulus pressure 52 bars. Attempted to inject seawater into F-12, stopped pumping at 190 bars. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 20:00 18/28 330° 3.7/5.9 350° 22:00 22/26 330° 3.6/5.7 340° 00:00 26/32 320° 3.3/5.7 340°" "On 2008-03-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Installed CRI check valve on to F-14. Greased valves on BOP. House keeping in the moon pool. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 02:00 17/20 320° 3.6/5.8 340° 04:00 30/34 320° 3.1/5.8 340° 06:00 15/18 340° 2.7/4.3 340° 07:00 29/33 350° 3.6/5.8 340°" "On 2008-03-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.0 hours. Operational details: WOW prior to retrieve the HP riser. Performed general maintenance and PM's. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 08:00 15/17 340° 4.2/6.7 340° 10:00 25/28 340° 3.9/6.3 340° 12:00 26/30 340° 3.6/5.8 340° 14:00 3.7/5.9 350° 07:00-10:30 No access to rig floor, due to exhaust fumes. 12:45-14:00 No access to rig floor, due to exhaust fumes" "On 2008-03-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW prior to retrieve the HP riser. Meanwhile RIH with test plug and landed of in sub sea WH. Attempted to pressure test against plug. POOH with test plug. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 16:00 23/26 330° 3.9/6.2 330° 18:00 23/27 360° 3.9/6.2 340° 16:30-19:00 No access to rig floor, due to exhaust fumes" "On 2008-03-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Performed general maintenance and PM's. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 20:00 3.8/6.1 340° 22:00 20/24 320° 4.0/6.3 340° 00:00 17/22 320° 3.9/6.3 340°" "On 2008-03-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: WOW prior to retrieve the HP riser. Not able to work at rig floor, due to exhaust fumes. Performed general maintenance and PM's." "On 2008-03-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW prior to retrieve the HP riser. Meanwhile re-RIH with test plug with polypack seals and landed of in sub sea WH. Pressure tested plug to 25/345 bars 5/10 min." "On 2008-03-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: WOW prior to retrieve the HP riser. Pressure tested BOP and TDS 20/345 bars 5/10 min. Performed derrick inspection. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 12:30 27/32 320° 4.5/7.2 340° 14:30 24/30 320° 4.6/7.3 340° 16:30 23/25 340° 4.6/7.4 340° 18:30 23/27 340° 4.2/6.6 340° 14:45-15:30 No access to rig floor, due to exhaust fumes" "On 2008-03-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: WOW prior to retrieve the HP riser. POOH with the test plug assy. Racked back string in derrick and laid out the test plug. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 16:30 23/25 340° 4.6/7.4 340° 18:30 23/27 340° 4.2/6.6 340° 16:30-18:30 No access to rig floor, due to exhaust fumes" "On 2008-03-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW prior to retrieve the HP riser. Prepared for N/D diverter. Checked tool for making up the Claxton tool. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 21:00 17/19 330° 4.2/6.7 340° 22:30 15/17 330° 3.5/5.5 340° 23:15 15/17 350° 3.1/5.0 340° 19:00-20:30 No access to rig floor, due to exhaust fumes 23:00-00:00 No access to rig floor, due to exhaust fumes" "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW prior to retrieve the HP riser. No access to rig floor, due to exhaust fumes." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box talk and N/D diverter and BOP. Had gas turbines shut down at 01:25 due to exhaust fumes blowing into the rig floor." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to M/U the Claxton tool." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Landed the Claxton tool on to the HPDR. Made Claxton tool to 1300 ft-lbs." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW prior to retrieve the HP riser. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 06:30 22/25 350° 3,4/5,4 340°" "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Shut in F-12 for production. Simultaneously prepared for retrieving HPDR BOP joint. Moved CRI hose line from F-12 to F-14. Installed hot stab, for releasing of riser TBC. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 08:30 13/15 020° 3,5/5,5 340°" "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Loosen BOP/Tension joint flange. At 11:15 confirmed production shut in. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 11:30 6/11 030* 2,6/4,1 340° 13:30 4/10 050° 2,2/3,4 340° 15:00 1/3 110° 2,1/3,4 350°" "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed horizontal tension support for riser in the moon pool." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Loosen the remaining 4 bolts on BOP/tension joint flange." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up the BOP joint and racked back one DP stand." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: R/U elevator on slings to allow, for laying out the Claxton tool with pup joint attached. Removed master bushing and outer ring." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled the BOP joint above the RT. Installed outer ring and the master bushing. Preserved the BOP joint flange. Laid out the BOP joint." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: R/D slings on elevator." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up riser lifting sub on one DP std." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box talk and RIH with C-type lifting sub and made up same to Tension joint. Simultaneously disconnected the Claxton tool from the BOP joint." "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed Spider. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 21:30 4/8 160° 1,7/2,7 350°" "On 2008-03-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Held tool box talk and applied 130 MT on to the string. Commenced to remove tension cylinders." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Continued rigging down the tension system. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 00:20 7/12 160° 1,3/2,1 360°" "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Held tool box talk and slacked of to 110 MT on the string. Released TBC as per Vetco procedure." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 95m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pulled HPDR tensinon joint and landed of in Spider. Racked back stand in derrick. Made up HPDR lifting sub. Pulled back first double HPDR with tension joint on top and landed of in Spider." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 95m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Disconnected flange bolt on HPDR flange and picked up double. Time Wind speed Wind direction Sea Wave direction Knots deg m deg 05:00 11/15 170° 1,5/2,4 360°" "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up handling flange type C to HPDR double B in rotary." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Landed double A on HTS cradle with simultaneous lift by deck crane and block. Re-slung double A and lifted to horizontal storage rack using deck crane." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled HPDR double B through rotary and placed coupling in working height above riser spider. Removed fairrings." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Landed off double B in riser spider. Broke bolts on flange. Inspected and preserved seal surfaces on flanges. Made up handling flange flange type C to double C." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Landed double B on HTS cradle with simultaneous lift by deck crane and block. Re-slung double B and lifted to horizontal storage rack using deck crane." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled HPDR double C through rotary and placed coupling in working height above riser spider. Removed fairrings." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Landed off double C in riser spider. Broke bolts on flange. Lifted off double C. Inspected and preserved seal surfaces on flanges. Made up handling flange type C to standard joint #1. Meanwhile ROV brushed wellhead seal area and installed VXG ring." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Landed double C on HTS cradle with simultaneous lift with deck crane and block. Re-slung double C and lifted to horizontal storage rack using deck crane." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Pulled HPDR standard joint #1 and placed coupling in working height above riser spider. Removed fairrings. Landed off HPDR standard joint #1 in riser spider. Broke bolts on flange. Observed loose skirt on TBC connector, bolts partly unscrewd and 2 bolts missing. Thightended bolts on TBC skirt." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up handling flange type C to HPDR lower pup joint." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Landed HPDR standard joint #1 on HTS cradle with simultaneous lift by deck crane and block. Re-slung double HPDR standard joint #1 and lifted to basket on main deck." "On 2008-03-27, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pulled HPDR lower pup joint and placed coupling in working height above riser spider. Removed fairrings. Landed off HPDR standard joint #1 in riser spider. Meanwhile installed debris cap on F-4 using ROV and tugger assist." "On 2008-03-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Broke bolts on flange between lower pup and stress joint." "On 2008-03-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 1.0 hours. Operational details: Due to findings made by production department, halted operation for inspection in wellhead area. A support bracket on the F-12 flowline/piping was found to be ripped off. Mærsk rig management decided not to start production due to the circumstances. Further investigation/assessment needed before starting production." "On 2008-03-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Landed HPDR lower pup joint on HTS cradle with simultaneous lift by deck crane and block. Removed handling flange. Re-slung HPDR lower pup joint and lifted to basket on main deck." "On 2008-03-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Installed handling flange type C on TBC joint. Pulled out TBC joint and laid down on HTS cradle with simultaneous lift by block and deck crane. Removed handling flange. Lifted TBC joint to basket on main deck." "On 2008-03-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: WOW for running production riser. Meanwhile: Cleared and tidied rigfloor. Brought F-4 flexible hose onto HTS. Held toolbox talk prior to transferring flexible hose to XMT deck." "On 2008-03-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 13.0 hours. Operational details: Waited on weather. Meanwhile : -Cleared XMT deck for reception of F-4 flexible hose -Transferred F-4 flexible hose to XMT deck -Suspended flexibel hose in roof and jacked to position for hook up -Landed BOP on test stump and made up NT-2 connector -Tested door seal on BOP" "On 2008-03-28, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather. Meanwhile : -Worked on hooking up flexible hose -Assisted production in equalizing across DHSV" "On 2008-03-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather. Meanwhile : -Worked on hooking up flexible hose -Tested BOP - 6 month 15 K test - had lekage on test stump -Changed gasket on test stump and made up NT-2 connector -Lifted F-4 XMT to moonpool -Transferred tension cylinders for F-14 to XMT deck" "On 2008-03-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 14.0 hours. Operational details: Waited on weather for running production riser. Meanwhile : -Performed 6 month BOP test to 15 K -Repaired 10 MT tugger in moonopol -Moved guide funnel to F-4 and installed debris cover -Performed derrick inspection" "On 2008-03-29, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: Waited on weather for running production riser. Meanwhile : -Performed repair of BX elevator -Lifted TBC joint to drillfllor -Performed pre-operational checks on TBC" "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 101m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held toolbox talk prior to lifting in tension joint. Removed BX-elevator. Installed 2 wire slings between bails and elevator. Picked up tension joint with deck crane and laid same on HTS cradle. Hooked up aft sling in tugger to get further in on drillfloor. Latched BX elevator around lift sub below 3 m pup joint. Lifted tension joint to upright position with simultaneous lift on deck crane and block." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 101m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed handling flange type F. Installed guide pins and landed tension joint on 3rd PR double. Made up connection using bolt tensioner tools. Pressure tested connection through test port 5 min / 345 bar using hand pump. Installed bolt protector caps. Installed fairrings." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Released BX elevator and removed slings. Installed BX elevator in bails. Re-latched tension joint. Removed spider and installed master bushing. RIH with tensioner joint, installed bowl and hung off riser on 3 m 5 1/2' pup joint." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up 5 1/2' landing stand. RIH with production riser on 5 1/2' DP. Guided TBC into guide funnel while observing with ROV. Used ROV C-guide for stabbing TBC. Positioned ROV with manipulator camera pointing upwards in guide funnel cut out window. Observed TBC relative to VX ring and top wellhead while comming down with production riser. Stopped riser motion when ~10 cm TBC swallow was obtained." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Detached lift sling on two points on each side of the hinge of the guide funnel. Unlocked hinge bolts and split guide funnel. Removed guide funnel by means of ROV and tuggers." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH with production riser and landed TBC on top of wellhead. Set down 10 MT. Ran hotstab and minireel hose along guidewire." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Established hot stab in port A and set valves on ROV lock panel to 'lock'. Verified TBC fully landed. Locked TBC by pressuring up through minireel to 3000 psi. Observed movement of indicator rods as prescribed. Maintained pressure for 15 mins. Set valves on ROV lock panel to parking position. Meanwhile assissted production in equalising across F-12 DHSV using cement unit." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed overpull test to 116 MT hookload / 20 MT overpull." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed hotstab and installed dummy stab. Moved hotstab to receptacle on panel B. Set valves to lower dog flush and injected hydraulic fluid / corrosion inhibitor through minireel." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed bleeder valve on top of tension joint running flange to prepare for pressure test." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Flushed and filled riser while venting air through valve on top of tension joint running flange. Closed valve. Lined up cement unit to standpipe and verified line-up by putting 15 bar on IBOP and opening same." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pressure tested production riser to 20/200 bar 5/10 min - ok. Pumped 680 liter and got full return when bleeding back. Observed for leaks around TBC with ROV - ok. Maintained 20 MT overpull on TBC while performing pressure test." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Reduced hookload to 107 MT / 10 MT overpull on TBC. Took measurement for contact ring relative to Centralizer deck. Meanwhile pumped corrosion inhibitor in TBC upper piston cavity through hotstab port B." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Unstabbed hotstab and installed dummy stab in receptacle B. Landed riser guide funnel on F-5 using ROV and tugger support. Installed hatches on all levels in wellhead module for slot F-3 and F-5." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to installing tensioner assembly." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.2 hours. Operational details: Hoisted tension ring and removed nylon guide in Centralizer deck. Installed centralizer and boat collision stool in Centralizer deck. Placed wooden beams on boat collision stool and landed tension ring on top. Installed contact ring below mark on riser contact grooves. Installed and assembled tension assy half hubs with shimms and made up tension ring lock plates. Connected 2 tension cylinders. Elevated tension assembly with tension cylinders and checked contact ring allignement. Made up contact ring. Connected 2 tension cylinders." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pressured up on tension cylinders to 4 x 90 bar (150 MT) and transferred tension from block to tension cylinders on Centralizer deck. Slacked off drillstring to obtain marginal overpull (~1 MT) at cutting height." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed centralizer assembly in Tensioner deck." "On 2008-03-31, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed Norse cutting equipment on riser. Barriered off Centralizer deck." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed Norse cutting equipment on riser." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Cut riser according to Norse procedure. Meanwhile : -Installed flood lights in derrick -Varco checked both PRS's with focus on falling objects -Painted tuggerchains and control panels on drillfloor -Tested Gray valve and FOSVs to 345 bar -Brought wellhead to drillfloor" "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Released top part of riser when cut obtained. Re-configuered cutting jig with 45 deg blades for machining bevel. Put protective ball on top of cut to avoid swarf falling into well." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Cut 45 deg bevel on riser circumference." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Rigged down Norse cutting equipment. Removed swarf and smoothed down cut. Marked deck for wellhead orientation." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Packed and removed cutting equipment. Cleared and tidied wellhead decks." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled landing stand and laid out handling flange and riser cut off." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to lowering WH with dual lift." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered WH to tensioner deck and landed same on top of riser." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: Orientated WH with valve stack pointing 45 deg relative to PORT/FWD. Pressure tested BT-seals to 35 bar - ok. Energized plastic in upper annd lower BT seal. Tested seals to 207 bar / 10 min - ok. Locked in 1000 psi after test. Energized slips with cap srews according to Vetco procedure. Pull tested WH with tugger - ok. Installed valves on A and B annulus outlets. Meanwhile loosended bolts on BOP NT-2 connector on stump. Made preparations to run BOP riser joint." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to installing BOP riser joint." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ran BOP riser joint using block and dedicated slings and landed on wellhead. Made up NT-2 connector. Retrieved lift slings." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to nippling BOP." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Nippled up BOP. Meanwhile prepared for installing diverter." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to installing slick joint and diverter." "On 2008-04-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Installed diverter in housing." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed diverter in housing." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Ran slickjoint and landed same on top of BOP. Removed running slings from bails and installed elevator." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: Function tested BOP shear ram - ok. RIH with test plug for testing BOP connection. Function tested BOP rams and annular - ok. Landed test plug in surface wellhead. Performed line test and verified line up by opening HCR with 35 bar - ok." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pressured up to 35 bar using cement unit - mismatch pumped vs theoretical volume. Suspected pressuring up against GT plug. Opened B-annulus valves to vent underneath plug and pressure dropped immediatly. Leakage observed across test plug despite steady pressure 35 bar indicating that plug did not vent into pipe when doing pressure test. Discussed situation - decided to re-attempt test while keeping B-annulus valves open." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Increased pumprate to 50 lpm and put 100 bar differential across plug, leakage decreased and pressure curve indicated that plug was sealing. Achieved steady pressure curve at 100 bar. Bled off pressure to 35 bar and held test for 5 mins (1,7 bar drop / 5 min). Steady fluid returns observed from B-annulus. Pressured up to 345 bar and tested connectors + inner A annulus valve for 10 min - 1,3 bar drop - ok. Shifted valves on A annulus. Held pressure and pressure tested outer A annulus valve for 10 min - 0,7 bar drop - ok. Pumped and bled back 43 liter (35=>345 bar). Still minor fluid returns from B-annulus outlet but gradually decreasing." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: POOH with 5 1/2' DP stand and test plug. Observed dirt/mud residues plug. Found pieces of steel in the mud residues. Strapped pipe and found landing point 20,45 m vs theoretical 20,81 m - but likely that plug landed too shallow." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up bowl protector to running tool and made up to stand of 5 1/2' DP. Meanwhile hooked up tension cylinders on BOP." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Installed bowl protector according to Vetco instructions. POOH with 5 1/2' DP stand and laid down RT. Meanwhile hooked up BOP tension cylinerders in moonpool." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to retrieving annulus insert." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Checked equipment prior to RIH." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up and made up annulus insert J-slot retrieval tool." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 76m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with retrieval tool on 5 1/2' HWDP landing string from surface to 76 m MD." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 76m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Mærsk crewchange. Held toolbox talk prior to continuing operation." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with retrieval tool on 5 1/2' HWDP landing string from 76 m to 120 m MD. Made up TDS and took torque readings wiith annular closed (200 psi on strip bottle). Torque 0,3-0,6 kNm at 5 rpm." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Tagged annulus insert at 139,68 m MD. Engaged J-slot and confirmed with 1 MT overpull." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Closed annnular and backed out insert with 3 lefthand turns. Max torque 5 kNm. Observed for pressure build up - none obeserved. Continued backing out annular insert with another 3 lefthand turns - observed 6' travel - ok." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Opened annular. Attempted to pull free - had 18 MT overpull. Continued rotating left and came free with annular insert." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flowchecked well - well static." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Emptied trip tanks. Displaced well to 1,03 sg completion fluid at 1000 lpm. Pumped a total of 26 m3." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke out TDS. POOH with annular insert on 5 1/2' HWDP landing string from 138 m MD to surface." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Broke out annular insert RT. Worked to free annular insert free from J-slot running tool due to debris jamming the sleeve." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up Smith 10 3/4' spear." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up spear to 5 1/2' HWDP (LS-1), checked serial no - ok. Broke spear and inserted 9,632' nominal grapple. Made up spear using rig tongs." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Made up adjustment sub setting tool to stand of 5 1/2' HWDP (LS-2), checked serial no - ok." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Performed extra washing trip in order to clean tie-back adapter. Made up bullnose/jet sub. RIH on 5 1/2' DP from surface to 140 m MD. Stepped up pumps to 3500 lpm / SPP 68 bar. Passed tie-back adapter and pulled back while pumping and rotating with 5 rpm. Pumped a total of 25 m3. Took returns to separate pit. POOH with jet sub." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up bowl protector RT and RIH on stand of 5 1/2' DP to 20 m. Caught bowl portector and POOH." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rig up 10 3/4' casing running equipment." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleared and tidied drillfloor prior to bringing in casing running equipment." "On 2008-04-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Installed BX-3 elevator, changed inserts and function tested same." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Moved Mærsk casing tong from drawwork deck storage and moved in front of IR." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Hooked up casing tong. Changed head on PDM to accommodate 10 3/4' casing. Moved HTS rollers from FWD to AFT end of cantilever. Dressed PS-30 casing with 10 3/4' inserts/dies. Removed masterbushing and installed PS-30 in rotary. Hooked up PS-30 slip. Programmed and tested casing tong - negative." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot casing tong / programming." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Function tested casing tong - ok." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up tie-back adapter and checked seals and acme thread. Installed tie-back adapter in slips. Secured same with dogcollar." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up first 10 3/4' joint and stabbed on to tie-back adapter. Had problems with Mærsk casing tong. Not able to get torque/turn curves on computer." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Investigated problem with casing tong." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Laid out tie-back adapter. Picked up joint #18 and #17 to test make up with Mærsk casing tong." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Attempted to make up connection, investigated missing torque reading on Mærsk system. Traced fault to be load cell or load cell amplifier." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Laid out jont #18 and #17 due to overtorque." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Rigged down Mærsk casing tong and frame." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Rigged up Odfjell casing tong and installed in rails in front of IR. Meanwhile held tollbox talk for re-installing safety net on FWD PRS." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Re-installed safety net around FWD PRS." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Powered up OWS casing tong. Installed travle cylinder." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Picked up tie-back connector and installed same in slips. Picked up 1 st joint and attempted to make up to tie-back adapter - not able to get torque/turn curve on Odfjell computer. Trouble shot situation. Changed gauges and valve on Odfjell tong." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 10 3/4' tie-back casing from surface to 108 m MD according to tally." "On 2008-04-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up and made up 10 3/4' hanger / adjustable sub assy. Landed hanger in slips. Broke off casing hanger handling tool. Checked casing hanger. Changed from BX3 to 5 1/2' BX elevator." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up pre-made 5 1/2' HWDP (LS-1) with 10 3/4' Itco spear with PRS. Attempted to make up stand to TDS - negative - slipped in TDS back up dies." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 119m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Broke off TDS from stand. Set down stand in PRS. Lowered TDS and inspected torque wrench dies, removed swarf from dies. Re-attempted make up to stand in TDS - ok." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Ran 10 3/4' Itco spear 3 m into 10 3/4' tie-back casing and latched same. Took up/down weight 82/79 MT. RIH with tie-back casing on 5 1/2' HWDP (LS-1). Put meter marks from casing hanger landing shoulder. Tagged with 4 MT at ~139,4 m, i.e. 30-40 cm shallow - no colour marks observed in WH B-annulus outlet. Re-attempted tag - same depth." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Evaluated situation. Checked drawings for potential hang-ups. Checked tally and joints left on deck - ok. Made two attempt to index pipe before tagging again - same depth. Sudden overpull of 14 MT observed after pulling some 30 cm above tag depth." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Decided to attempt to screw in 1-2 turn in order to verify tie-back adapter depth. RIH and tagged approx 10 cm deeper than earlier. Observed lower orange and white band in B-annulus outlet. Measured required distance for adjustment sub travel (15') and decieded to continue according to plan." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Set torqe limit to 2700 Nm. Made 3 attempts to enter tie-back adapter. Entered tie-back adapter on 4th attempt and observed weight increasing about 3-4 MT for each turn. Slacked off to neutral (80 MT) for each turn achieved. String stalled out at 2700 Nm after 5+ turns achieved. Took 10 MT overpull. Rotated at 1 rpm. Attempted make up to 10 000 Nm (optimum torque) - spear started to slip at 5500 Nm. Re-engaged spear. Adjusted torque setting to minimum torque 6600 Nm -spear started to slip at 5500 Nm. Re-enaged spear. Set torque limit to 10 000 Nm, increased rotation to 3 RPM. String stalled out on 10 000 NM (optimum torque) - ok." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Took 30 MT overpull to check pre-tension in casing towards datum. Streched pipe approx 2' and observed lower white band through B-annulus outlet." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged down Odfjell casing tong and removed PS-30 slips. Installed masterbushing and bowl." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Jammed torque wrench on TDS. Inspected equipment and found that wrong die-holders had been installed. Changed die-holders." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up adjustment sub activation tool." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with adjustment sub and located same at 28,4 m MD. Checked serial numbers on pipe. Made up TDS." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressured up on drillpipe to 140 bar to activate horizontal dogs. Pulled back 0,4 m and confirmed engaged in vertical dog profile by 9 MT overpull. Rotated string with 22 righthand turns. Observed colored band through B-annulus outlet to confirm adjustment sub collapsing. Increased overpull to 30 MT and continued rotating until TDS stalled out on 9 kNm and overpull reduced. Slacked off string to 28,4 m MD mark and waited for 2 min. Bleed off pressure on DP. Obtained a total of 17' travel on adjustment sub." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with adjustment sub activation tool and racked back in derrick." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made up Drillquip straddle cup tester." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with straddle cup tester and located same at 28,4 m MD across metal seal in adjustment sub. Meanwhile held toolbox talk for pressure testing." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up cement unit on standpipe. Performed line test to 380 bar." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Pressure tested adjustment sub (metal seal) to 380 bar / 10 min - ok. Kept B-annulus open throughout test." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with straddle cup tester from 28,4 m and located same across tie-back adpater at 140,5 m MD." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Filled pipe with approx 1,8 m3 packer fluid prior to testing. Pressured up to 380 bar - observed leakage from B-annulus outlet - not able to obtain test." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pulled back 10 m to put cuptester in blank pipe to test tool. Pressured up - not able to obtain test - straddle cup test leaking." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH with straddle cup tester from 130,5 m MD to surface. Laid out cup tester and inspected same. Found no tears or flaws, but OD reduced significantly (9,85'/9,70' vs originally 10,13')" "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging casing running equipment." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rigged up casing running equipment. Found a yellow sheared allen bolt on walkway along drillfloor. Suspended operation and evaluated situation." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Isolated aft PRS and TDS and inspected same with manrider. Found origin of bolthead to be from backside of aft PRS upper grip head." "On 2008-04-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Parked aft PRS for repair. Performed repair work on aft PRS. Broke out and re-thightended in total 24 allen/hex bolts with prescribed momentum (600 ft lbs). Replaced broken bolt. Meanwhile : -Installed BX3 elevator in bails -Brought Vetco/BOT equipment to cantilever" "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Repaired aft PRS. Meanwhile prepared for rigging casing running equipment." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged up Odfjell casing tong adn PS-30 slips dressed for 10 3/4' casing." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for running 10 3/4' hanger running tool on 10 3/4' casing." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up 10 3/4' x 1502 swedge to 8 m 10 3/4' casing joint. Laid out casing joint." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Suspended operation due to reported fumes. Wind direction 330. Assessed situation. Decided to resume operation." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 10 3/4' casing hanger RT and hung off in slips. Picked up joint of 10 3/4' casing and made up to RT. Picked up joint with pre-made swedge." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up pup joint with pre-made 1502 swedge. RIH and landed casing hanger RT at 20 m MD. Set of weight of landing string. Entered hanger RT threads using chain tong. Made up RT with 9 lefthand turns using casing tong." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pressure testing." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged up 1502 chicksan from swedge to cement hose hub on drillfloor." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to cement pump and flushed lines. Performed line test to 380 bar - ok. Exhaust fumes detected on drillfloor." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressured up on cement unit and tested upper tie-back/adjustment sub/tie-back adapter to 380 bar /10 min - ok. Pumped and bled back 587 litres." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Exhaust fumes on drillfoor and drillers cabin. Suspended drillfloor operations. Checked wind and conditions every 30 min. Monitored well from shaker control room. Meanwhile : -Cleaned and tidied in moonpool -Cleaned and tidied in wellhead module -Housekeeping in heavy tool store 21:30 - shut down gas turbines to get working conditions on drillfloor." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Resumed work on drillfloor. Broke out casing hanger RT with 10 turns. Unable to latch elevator on 10 3/4' casing, had to use singel joint elevator and tugger. Pulled 10 3/4' landing string. Broke out RT. Broke out 1502 swedge." "On 2008-04-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rigged down casing tong." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Rigged down casing tong. Removed PS-30 slips. Observed dropped object on drillfloor - hex/allen bolt head from aft PRS. Suspended operations for investigation. Fenced off drillfloor." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Inspected aft PRS. Discussed way forward. Parked and isolated aft PRS. Secured backside of aft PRS gripper head with cover and trailer straps for dropped object prevention." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Resumed operations. Removed BX3 elevator and installed 5 1/2' DP elevator. Cleared drillfloor from casing handing equipment." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran 2 x 5 1/2' DP singels and made up to MS-seal running tool. Meanwhile laid out DP singels on deck to cater for continued operations." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Made up control lines to MS-seal RT. Function tested and adjusted dogs and stroke on MS seal RT." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Locked MS seal running tool in surface WH, observed 0,4 l return - ok. Performed 10 MT overpull to confirm latch - ok. Set MS seal assembly by applying 4300 psi. Observed 1,62' travel / 3,5 liter returned fluid - ok." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressure tested MS seal through test port in surface wellhead to 380 bar / 10 min - ok." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released dogs in MS seal RT by rotating 5 turns to the right." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with MS seal RT on 5 1/2' DP stand. Broke RT tool and laid down." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbx talk before running bowl protector." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Made up bowl protector RT. RIH and set bowl protector at 20,10 m MD." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out RT and laid down same. Laid out 2 joints of 5 1/2' DP." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held toolbox talk and prepared for running casing drift. Experienced problems with programming PDM." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Troubleshot PDM. Unable to travel to port aft pipe bay." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Tested PDM - ok. Tested stabbing. Discussed issues related to pipe handling." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up 9,567' casing drift and made up to 5 1/2' HWDP single." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 9,567' casing drift from surface to 140 m MD on 5 1/2' HWDP singels. Re-arranged pipe on cantilever deck." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 245m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 9,567' casing drift from 140 m to 245 m MD on 5 1/2' DP singles. Detected exhaust fumes on drillfloor." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 245m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Exhaust fumes on drillfloor. Made up TDS and spaced out for BOP. Abandoned drillfloor. Shut down one of the gas turbines to reduce exhaust fumes." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 580m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Resumed operations. Continued to RIH with 9,567' drift from 245 m to 580 m MD." "On 2008-04-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 223m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: POOH with 9,567' drift on 5 1/2' DP from 580 m to 223 m MD. Laid out singles on deck when pulling out. Performed kick drill." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH with 9,567' drift on 5 1/2' HWDP from 223 m to surface. Laid out singles on deck when pulling out. Observed dropped object on drillfloor - half crest of external lock ring / simmer ring for pin, 70 mm x 2 mm / 10 grammes. Suspended operations for investigation. Fenced off drillfloor." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Inspected rig equipment. Found source of dropped object to be cherry picker main hydraulic lift cylinder. No risk of larger dropped object from equipment - lock ring served no purpose." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Resumed operations. Held toolbox talk. Made up GTV pulling tool to stand of drillpipe hanging in block. Ran stand carefully through BOP. RIH to 80 m MD on 5 1/2' HWDP singles. Observed leakage on BX-elevator." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 80m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Fixed BX elevator. Changed 3 ea hydraulic hoses/fittings running from TDS to BX elevator." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with GTV pulling tool from 80 m to 130 m MD on 5 1/2' HWDP singles." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with GTV pulling tool from 130 m to 600 m MD on 5 1/2' singles." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 615m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Tagged plug with 2 MT at 615 m MD." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 615m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pulled back 1 joint and made up DP to TDS. Displaced his-vis at 2400 lpm. Pumped a total of 37 m3 1,03 sg completion fluid." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 615m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to releasing plug." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 615m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Due to unsactisfactory cleanliness of completion fluid, pumped additional 26 m3 at 2400 lpm." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 610m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Latched onto plug and confirmed by 10 MT overpull. No pressure observed on standpipe but slight gain in triptank indicating equlized plug. Rotated at 5 rpm righthand while holding 3 MT overpull, released plug with 10 turns, no gain observed. Pulled back 5 m and waited for elastomer element to relax." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 610m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with plug to 620 m MD to confirm released. Pulled 5 1/2' single and gained 0,2 m3 in trip tank due to swabbing plug." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 578m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Pulled 3 x 5 1/2' singles while pumping at 200 lpm. Swabbing stopped when plug entered 10 3/4' casing." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: POOH with GTV plug on 5 1/2' DP singles from 578 m to 145 m MD." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: POOH with GTV plug on 5 1/2 HWDP singles from 145 m MD to surface." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out and laid down GTV plug and pulling tool." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Made up secondary bowl protector pulling tool. RIH and latched secondary bowl protector. Strapped pipe while POOH, measured 20,45 m to tubing hanger landing shoulder. Made up kick assembly." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging up tubing running equipment." "On 2008-04-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Positioned HTS and moved rollers on cantilever. Cleared drillfloor. Positioned control line reel on fwd pipe setback. Meanwhile installed NPR plug with ballseat in tailpipe joint." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Re-arranged kick joint. Re-booted PDM and tested same." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: Changed to BX3 elevator. Positioned Odfjell casing tong on rails in front of IR, hooked up same to panel on aft pipe setback. Removed master bushing and installed PS-30 slips. Bulit scaffolding platforms for dropped object protection above tong operating panel and control line reel panel." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk before running 7' tubing." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 37m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Picked up completion assy#1. Function tested ratcheting mule shoe - ok. Checked seals and rupture disk - ok. Hung off assy#1 in slips. Picked up and made up joint #265 with presintalled NPR plug / ball seat 1,98 m from collar. Picked up and made up 1 joint of tubing. Picked up and made up completion assy#2 / SB-3 injection packer. Checked packer element and slips." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 72m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 37 m to 72 m MD. Checked self filling of tubing - ok. Raised doubt about torque read back on jam computer." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 85m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Investigated deviation between tong gauge and jam coumputer. Found that wrong transducer was set up in the jam computer, with the consequence that the casing tong output too low torque." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 31m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Held toolbox talk prior to laying out undertorqued tubing. Laid out tubing joints #258 to #262." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 31m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Installed pipe guide in PS-30 slips." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 31m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Inspected box on joint #263 and found it to be damaged / gaulled. Broke off box and inspected pin thread - ok. Made up new coupling collar on joint#263 - ok." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 31m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up back-up assy#2 SB-3 injection packer." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 36m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Picked up and made up back-up assy#2 SB-3 injection packer, RIH and hung off in slips." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Picked up and made up 7' tubing joint. Raised doubt about torque setting on tong. Stopped operations for investigation." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 6.8 hours. Operational details: Found casing tong to be programmed with wrong torque values. Optimum torque set to 15660 ft lbs instead of 15660 Nm. Two tubing connections on assy#2 overtorqued. No back-up assembly available. Discussed situation. Evaluated and discussed further actions with town. Got confirmation that VamTop thread should be good within 30% overtorque. Decided to do drift run through overtorqued couplings to verify no deformation or restrictions. Meanwhile : -Repaired handrails and kick plates in derrick -Removed 10 allen/hex bolts from fwd PRS" "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 48m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Rigged up tugger with Seawell adjustable drift sub. Performed drift run through 1st coupling (13,2 m) to 5,977' - ok. Perfomed drift run through assy#2 and 2nd coupling (21,2 m) to 5,80' - ok." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 48m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to continuing tubing running. Verified Odfjell jam computer with correct torque values." "On 2008-04-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 238m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 48 m to 238 m MD. Running speed 30 sec per joint. Checked self filling of tubing - ok." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 561m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 238 m to 561 m MD. Running speed 30 sec per joint. Checked self filling of tubing - ok." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 561m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Handover for short change of Mærsk crew. Held toolbox talk for continued operations. Greased PS-30 and elevator." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 750m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 561 m to 750 m MD. Reduced running speed to 1 min per joint in 9 5/8' casing. Checked self filling of tubing - ok." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 834m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 750 m to 834 m MD." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 834m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Bad make up on joint #189, laid out same. Broke out box on joint #190. Inspected pin and made up new box on joint #190. Moved mobile cherry picker to aft part of drillfloor for use on aft PRS." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 963m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 834 m to 963 m MD." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 963m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Bad make up on joint #177, laid out same. Broke out box on joint #178. Inspected pin and made up new box on joint #178." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1345m. The activity was categorized as 'completion -- completion string' and lasted for 4.2 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 963 m to 1345 m MD." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1333m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Not able to make up joint #146, laid out same. Inspected box - negative. Laid out joint 145." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1434m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 1333 m to 1434 m MD." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1434m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Inspected threads on joint #134 - negative - laid out joint." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1455m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 1434 m to 1455 m MD." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1455m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Inspected threads on joint #129 - negative - laid out joint. Mærsk crew change and toolbox talk." "On 2008-04-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1743m. The activity was categorized as 'completion -- completion string' and lasted for 4.2 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 1455 m to 1743 m MD." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1938m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 1743 m to 1938 m MD." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1938m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Bad make up on joint #90, laid out same. Washed and inspected threads on pipedeck. Applied API mod lubeseal dope to pin ends on pipedeck." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2164m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: RIH with 7' 29# S13%Cr tubing from 1938 m to 2164 m MD." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2164m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up completion assy#3 DHSV. Counted joints left on deck 84 - ok." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2164m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Picked up completion assy#3 DHSV. Made up completion assy#3 and ran through RT. Isolated pipe guides on PS-30 slips." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2164m. The activity was categorized as 'completion -- test scsssv' and lasted for 2.0 hours. Operational details: PU and installed one tubing joint above TRSCSSV assembly. Flushed control line. Connected control line to TRSCSSV and leak tested to 570 bar/10 min. Bled pressure down to zero. Checked slips alignement. Made guide arrangement for control line from tubing to CL drum. Pressured up control line to 420 bar to keep TRSCSSV open while RIH." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2645m. The activity was categorized as 'completion -- completion string' and lasted for 8.5 hours. Operational details: RIH with 7' 29# S13%Cr tubing with CL and clamps from 2164 m to 2645 m MD. Up weight 172 MT / down weight 141 MT. Distance between up and down weight was 0.3 m." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2645m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Held tool box talk before entering 7' liner." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2645m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Lined up to pump down kill line and to be able to observe overflow from top of tubing. Verified line up with 15 bar." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2649m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: RIH with 7' 29# S13%Cr tubing with CL and clamps from 2645 m to 2649 m MD. Closed annular BOP at 280 psi. Attempted to reverse circulate, neg. Leaked through annular. Closed annular BOP at 580 psi. Reverse circulated using clean brine at 50 lpm / 3 bar and 100 lpm / 3.5 bar to get a reference. Observed returns. Stopped circulating and opened annular BOP." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2662m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: RIH with 7' 29# S13%Cr tubing with CL and clamps from 2649 m to 2659.8 m MD. Performed reverse circulation exercise 50-100 lpm / 3.5 bar. Moved string down in 30 cm increments from 2659.8 m to 2662.2 m and repeated reverse circulation exercise with same pressure response (50-100 lpm / 3.5 bar)." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2662m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: POOH with 7' 29# S13%Cr tubing with CL and clamps from 2662.2 m to 2644 m MD. PU 2.89 m pup joint to space out to be able to close annular without a coupling or a clamp in the interval. RIH with 7' 29# S13%Cr tubing from 2644 m to 2662.2 m MD." "On 2008-04-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2663m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Performed reverse circulation exercise 50-100 lpm / 3.5 bar. Moved string down in 20 cm increments from 2662.2 m to 2662.8 m." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2664m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Performed reverse circulation exercise 50-100 lpm / 3.5 bar. Moved string down in 20 cm increments from 2662.8 m to 2664.3 m. Had 1 bar increase in pressure from 2663.4 m. Had overflow response on tubing while RIH at 2664.3 m before flow was cut off - indicating that the lower most seal had entered 7' liner PBR. Confirmed the situation by reverse circulating 50 lpm up to 8.6 bar with no returns. Stopped circulating. Measured 7.24 m stick-up. TOL found at 2662.85 m." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2664m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: POOH with 7' 29# S13%Cr tubing with CL and clamps from 2664.3 m to 2631 m MD. Calculated and performed space-out with pup A,D,E, and F, leaving lower most seal on seal stem stung in by 75 cm (2.2 m from end of string)." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2643m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box talk prior to PU tubing hanger. PU and MU tubing hanger with handling tool to space-out pup joints sitting in the slips. Secured control line with clamp on pup joint coupling. RD control line cable sheave and terminated cable to TH. Wrapped control line 5 times and fed control line thru TH using swagelok fittings above and below hanger. Plugged off penetration holes in TH with 3/8' NPT blind plugs. Leak tested TH fittings through 1/8' test port to 35 bar/5 min." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2643m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Leak tested TH fittings through 1/8' test port to 380 bar/10 min using BOT pump." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2643m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Held tool box talk. Lifted TH hanger above slips. Removed PS30 slips and installed master bushings. Installed C-plate and landed TH in C-plate. BO handling tool and LO same." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2647m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed communication collar onto hanger and made 5 right hand turns until it shouldered out on TH. Wrapped CL 3 times around hanger neck. Connected TRSCSSV CL to 1/4' communication port at btm of communication collar. PU tubing hanger RT with 7' #29 pup joint. Backed out THRT piston retaining screws and MU THRT to communication collar with 8 turns left hand rotation. Connected TRSCSSV CL to 1/4' communication ports on top of THRT." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2647m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Leak tested TRSCSSV control line to 570 bar/10 min using BOT test pump. Kept 520 bar pressure on line while RIH. Screwed in THRT piston retaining screws. Control-measured RT and pup-joint lengths." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2647m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Stopped trip tank and drained production riser." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Removed C-plate. Ran in with THRT below rotary. Installed bowls. PU and MU joints for landing string. Up weight 173 MT / down weight 144 MT. RIH with 7' 29# S13%Cr tubing, TH and THRT on landing string from 2647 m to 2665,2 m MD. Got indications when ratcheting muleshoe and seals entered 7' liner PBR. Landed TH on no-go shoulder in surface tubing head. SO weight. Leak tested TH in port 1 and 2 on surface well head to 70 bar/5 min to verify that TH had landed correctly. Engaged TH lock down ring by applying 207 bar. Performed pull test with 15 MT overpull to verify TH lock down. SO weight." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested TH seal through test port 1 and 2 on surface WH to 35/380 bar for 5/10 min using Vetco pump." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- test scsssv' and lasted for 2.5 hours. Operational details: Held toolbox talk. Installed 7' #29 Vam Top P x 5 1/2' FH B swedge and 2' Wetco pump in sub with lo-torque valve. RU cmt hose/cmt unit to lo-torque valve and flushed CMT line to rig floor. Performed line test to 345 bar / 10 min using packer fluid. Observed 1.6 bar drop (0.46%). Performed line test without cmt hose and observed 0.3 bar drop." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Pressured up tubing against NPR plug at 2648 m MDRT to 30 bar / 10 min to check tubing integrity before initiating packer setting. 70 ltrs pumped. Kept 570 bar on TRSCSSV CL. Observed 0.3 bar drop. Closed TRSCSSV. Bled down to 5 bar above TRSCSSV and function tested TRSCSSV for 10 min. Bled back 36 ltrs. Observed 0.2 bar drop. Equalized and opened TRSCSSV." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Continued to pressure up tubing to 345 bar. Held pressure for 15 min to set SB-3 packer and test tubing. 1050 ltrs pumped. Observed 1.5 bar drop (0.43%)." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Bled down pressure to 320 bar. 60 ltrs bled back. Closed TRSCSSV and bled off pressure above to 250 bar. Bled back 35 ltrs. Inflow tested TRSCSSV with 70 bar diff / 30 min. Inflow test OK. Bled off pressure above TRSCSSV to 10 bar. Bled back 120 ltrs. Inflow tested TRSCSSV with 310 bar diff / 30 min. Inflow test OK. Equalized and opened TRSCSSV using 157 ltrs. Bled off pressure in tubing to zero. Bled back 800 ltrs." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: RU cmt hose/cmt unit to A-annulus to leak test packer from above and TH from below. Opened B-annulus to vent. Performed line test to 35/380 bar for 5/10 min pumping brine at 70 lpm. Observed 1.8 bar drop (0.47%) on high pressure test." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2665m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Pressured up A-annulus to leak test packer from below and TH from below to 35/380 bar for 5/10 min pumping brine at 70 lpm. Kept tubing open on drill floor and 570 bar on TRSCSSV CL. Pumped 125 ltrs and observed 0.2 bar drop on low pressure test. Pumped 1130 ltrs (total) and observed 2.1 bar (0.5%) drop on high pressure test. Had flow on both tubing and B-annulus while pressuring up A-annulus due to ballooning effect. No flow observed when pumps was shut in. Bled pressure down to zero and had 1100 ltrs in return. Closed TRSCSSV." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Held tool box meeting. Released landing string by 9 right hand turns. POOH and LD landing string. Changed to 5 1/2' handling equipment." "On 2008-04-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Held tool box meeting. PU and MU XO 5 1/2' FH box x 3 1/2' IF box to centralizer / BPV running adaptor / BPV. RIH and landed BPV on 5 1/2' DP in TH at 20.3 m. Sat down string weight to extend locking keys and energize seals. Rotated string 8 1/2' turns clockwise to lock mandrel and free running adaptor in J-slot. POOH with running string and LD RT." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: POOH with running string and LD RT." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: RD completion handling equipment." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: PU 2 joints of 5 1/2' HWDP and RIH and drained riser." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: ND and pulled diverter." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Continued ND diverter. Went trough SJA and procedure with day crew. Attached slings to slick joint. Prepared barriers, handrails and slings. Lifted out diverter. Installed outer ring and master bushings. Loosened nuts on slick joint." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box talk and reviewed SJA and procedures. Disconnected tension cylinders in WH module." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: ND NT2 connection on BOP. Informed production department to shut in well at 12.30." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Waited on production to shut in well. Meanwhile removed 2 HP hoses connected to WH." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: ND slick joint and BOP." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Dismantled scaffolding on NT2 connection in moonpool and installed slings on riser. RU for disconnecting riser NT2 connection and disconnected same." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Dismantled scaffolding in moonpool. PU riser and terminated control lines on well head. Installed carrier on HTS. Installed hatch on weather deck and master bushings on rig floor. Hoisted riser to rig floor and retracted same." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.8 hours. Operational details: Disconnected control lines from communication collar and hoisted same to rig floor. Installed hatch in moonpool. Installed outer ring and master bushings on rig floor. Installed anti vibration ring on TH. Removed one control line exit block on multi bowl. Unwrapped required length of CL around TH neck and fed control line through dedicated port on multi bowl. Fed high pressure packings and fittings onto CL and MU fittings to threads in multi bowl. Installed dart in BPV in TH by hand. Installed 137 VG seal ring on top of multi bowl and VG 63 seal ring on top of TH." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.2 hours. Operational details: Removed hatch to F-4. Lowered spacer spool down from rig floor with TDS until NT2 box connector landed out on top of WH. MU locking dogs until connection leveled out. MU actuation screws with 800 ft-lbs. Disconnected slings and removed same. Pressure tested and energized BT seals through ports 7/8. Tested VG 63 connection trough test port 9/10 to 35 bar/5 min. Tested TH void, grafoil seals and BT seals 35/380 bar for 5/10 min via test port 5/6. MU ferrule swagelock fittings for CL. Installed seal rings and CL exit block. Installed seal ring on top of spacer spool." "On 2008-04-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.5 hours. Operational details: Skidded cantiliver 1.5 m starboard and as far aft as possible to be able to possition crane for lifting XMT." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box meeting. Connected crane hook to one of the two chackles in the end of the chain hoist and wire sling. Disconnected transport plate. Lifted XMT to wireline deck and landed it on wooden beams, where it hung suspended in crane hook and resting on wooden beams with 1 MT." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.2 hours. Operational details: Skidded rig to sea fastening position to gain access for lifting XMT with the port aft deck crane." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box meeting. Attempted to lift XMT from wireline deck to F-4 wellhead. Could not reach F-4. Decided to skid further to starboard." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded 0.6 m further starboard and reached max skidded position starboard and fwd (sea fastning position)." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.0 hours. Operational details: Unable to reach F-4 and F-5 with port aft deck crane. Evalutated alternative methode for landing of XMT. Meanwhile held toolbox meeting and went through procedures and SJA with day crew." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Skidded port and aft out to F-4. Meanwhile lined up from CMT onto F-12 kill valve. Lined up over choke manifold to equalize above TRSCSSV. Tested lines. Equalized TRSCSSV with 84 bar and opened same. Started production from F-12." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Held time-out for safety. Talked about everyones right to stop the operation if anything is unclear or confusing. Went through operational plan and safety aspects involved." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Installed staircase to cantiliver." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed big moonpool hatch and lowered XMT to moonpool. Re-installed hatch." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.0 hours. Operational details: Transfered XMT from turtle to weather deck and skidded cantiliver to port and fwd to position XMT in center." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Waited on production to shut in well." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Attached TDS to XMT. Positioned and disconnected base plate." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded rig fwd and port to position XMT over F-4 for final installation. Meanwhile bled down all pressures on F-12 to zero bar." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Moved hatch on weather deck to allow XMT to pass through. Lowered XMT until 1 m above F-4 spacer spool." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held tool box meeting. Lowered XMT on to spacer spool with TDS and verified correct orientation. MU graylock connection. Re-built scaffolding around XMT for proper working environment. Checked alignment of flanges between flow hose and XMT. Pressure tested seal ring 35 bar/10 min through test port 3/4 on spacer spool to confirm proper seal." "On 2008-04-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Installed flow line spool. Disconnected lifting wire from TDS. Connected flexible flow line to flow line spool. Re-installed hatch." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.8 hours. Operational details: Postphoned XMT tests to assist production to start up F-12. Lined up from CMT onto F-12 kill valve. Lined up over choke manifold to equalize above TRSCSSV. Tested lines. Equalized TRSCSSV and opened same. Started production from F-12." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Held tool box meeting. Opened HMV with Seawell test pump. Lined up from cmt unit and connected hose on KWV. Performed line test to 20 bar for 5 min." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Trouble shoot line up from cmt unit through valves and hose from moonpool to KWV due to failing line test. Detected exhaust fumes in WH area." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Exhaust fumes in well head area. Abandoned WH. Shud down on of the gas turbines to reduce exhaust fumes." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed line test to 30/380 bar for 5/10 min against KWV. 2.2 bar drop on high pressure test." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Attempted to pressure test XMT body and VG 63 ring to 30/380 bar for 5/10 min against dart in BPV. Failed due to leaking dart/BPV." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Held tool box talk. Removed XMT tree cap. Opened HMV. RIH with retrieving tool for dart on stinger and retrieved dart. POOH with dart. RIH and installed new dart. Flushed XMT. Closed HMV." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Attempted to pressure test XMT body and VG 63 ring to 30/380 bar for 5/10 min against dart in BPV. Failed due to leaking dart/BPV." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled dart and BPV. Installed a new BPV and dart. Flushed XMT." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested XMT body and VG 63 ring to 30/380 bar for 5/10 min against dart in BPV. 2.5 bar drop on high pressure test." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pressured up to 130 bar against BPV & dart. Close MMV and bled off pressure above MMV to 10 bar. Inflow tested MMV to 120 bar differential pressure for 15 min. 1.9 bar drop. Equalized pressure above MMV. Opened MMV and closed HMV. Bled of any pressure above HMV to 10 bar. Inflow test HMV to 120 bar differential pressure for 15 min. 2.4 bar drop. Equalized pressure across HMV. Opened HMV. Bled off pressure. Closed valves." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed XMT tree cap. Opened HMV. RIH with retrieving tool for dart on stinger and retrieved dart. POOH with dart. Pulled BPV from TH." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Re-installed XMT tree cap. Close HMV. Test three cap 380 bar/10 min against SV. Bled off pressure." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure test TRSCSSV CL exit block to 570 bar/15 min, using BOT pump. Test ok. No indication that TRSCSSV opened. Bled off 155 ml on line." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Evalutated options for flushing flowline and made plan for flowline test. Handover with new crew." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box meeting. Hooked up flexible hose and lined up for pressure testing flowline. Flushed through XMT PWV, KWV and lo-torque to cement unit with pot-water." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Attempted to pressure test flow line and XMT to 30/345 bar for 5/10 min. Observed leak at flange on flexible hose." "On 2008-04-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Inspected, greased and torqued up flange on flow line flexible hose. Meanwhile worked on varco bolts on AFT PRS and installed tension cylinders on F-14." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Inspected, greased and torqued up flange on flow line flexible hose. Meanwhile worked varco bolt on AFT PRS and installed tension cylinders on F-14." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Flushed through XMT to cmt unit prior to testing flowline. Pressure tested flow line and XMT to 30/345 bar for 5/10 min. 1.1 bar drop on low pressure test and 1.7 bar drop on high pressure test." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: Commisioned XMT. Meanwhile worked on varco bolts on AFT PRS and installed tension cylinders on F-14." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Installed instrumentation on F-4 XMT. Connected umbilical to bulk head plate. Meanwhile changed out chain on HTS, emptied trip tank and repaired sensor on gate valve shakers. Started to change out one tension cylinder on F-14. Carried out work scope with climbers in derrick." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Waited on production to restart after production shut-down." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Energized instrumentation on XMT. Meanwhile changed out one tension cylinder on F-14 and cleaned area. lined up from cement unit onto F-12 kill valve. Lined up over choke manifold. Equalized TRSCSSV with 94 bar and opened same. Started production from F-12. Carried out work scope with climbers in derrick." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Function tested XMT pressure transmitters. Meanwhile retrieved base plate from weather deck to moonpool. Carried out work scope with climbers in derrick." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Mounted umbilical termination plate on XMT. Meanwhile performed housekeeping on cantilever. Carried out work scope with climbers in derrick." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Tested annulus pressure transmitters on XMT. Meanwhile worked on Varco bolts on aft PRS. Built suspended scaffolding for repair on fwd PRS. parked and landed BOP on test stump." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Function tested PWV and HMV on XMT with process operator present. Feed back on valve position to process control room read OK. Meanwhile continued building suspended scaffolding for fwd PRS in paralell with securing bolts on aft PRS." "On 2008-04-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Commenced commisioning of XMT. Verified documentation from Vetco Gray and Aibel. Performed pre-commisioning checks. Meanwhile continued building suspended scaffolding for fwd PRS in paralell with securing bolts on aft PRS. Started to lift parts for fwd PRS onto scaffolding." "On 2008-04-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Performed pre-commisioning checks of valves on XMT. Function tested MMV and SV and XMT with process operator present. Feed back on valve position to control room read OK. Meanwhile continued building suspended scaffolding for fwd PRS in paralell with securing bolts on aft PRS." "On 2008-04-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Performed pre-commisioning checks of valves on XMT. Function tested MMV and SV and XMT with process operator present. Feed back on valve position to control room read OK. Meanwhile continued building suspended scaffolding for fwd PRS in parallell with securing bolts on aft PRS." "On 2008-04-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 10.0 hours. Operational details: Commisioned XMT. Meanwhile performed derrick inspection with climbers and worked on BOP." "On 2008-04-16, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 7.0 hours. Operational details: Waiting on WL equipment and personnel to arrive on rig. Completed commisioning of XMT 38 hrs ahead of plan. Meanwhile erected scaffolding platform for fwd PRS and performed 3-montly maintenance on BOP." "On 2008-04-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 6.0 hours. Operational details: Waiting on WL equipment and personnel to arrive on rig. Meanwhile erected scaffolding platform for fwd PRS and performed 3-montly maintenance on BOP." "On 2008-04-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 5.0 hours. Operational details: Waiting on WL equipment and personnel to arrive on rig. Meanwhile performed derrick inspection with climbers and performed 3-montly maintenace on BOP." "On 2008-04-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Prepared for RU wireline equipment and tested dual and trippel BOP's. Meanwhile equalized above DHSV on F-12 with cmt unit to re-start production. Observed leak in F-12 XMT. Meanwhile performed derrick inspection with climbers and performed 3-montly maintenace on BOP." "On 2008-04-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 6.5 hours. Operational details: Prepared for RU wireline equipment and tested dual and trippel BOP's. Meanwhile identified leak on F-12 XMT to be in MEG injection valve. Meanwhile performed derrick inspection with climbers and performed 3-montly maintenace on BOP." "On 2008-04-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Prepared for RU wireline equipment and tested dual and trippel BOP's. Meanwhile continued to work on scaffolding platform for fwd PRS." "On 2008-04-17, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.2 hours. Operational details: Held tool box meeting. Spotted WL equipment on rig floor and hooked up BCU and pump skids. Prepared riser and BOP for lifting down to moonpool area. Meanwhile changed MEG injection valve on F-12 and re-tested valve to 325 bar/30 min." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Spotted WL equipment on rig floor and hooked up BCU and pump skids. Prepared riser and BOP for lifting down to moonpool area. Meanwhile equalized above DHSV on F-12 with cmt unit to re-start production. Production on F-12 started 02:00. Meanwhile built scaffolding bridge from cantiliver to Schlumberger WL deck (port aft leg)." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.8 hours. Operational details: Held tool box meeting. Hooked up chicksan line in moonpool from cmt unit to both F-12 and F-4 with seperate high pressure hoses. Lifted off hatch on F-4. Leak tested line from cmt unit to XMT KWV with LTV4 closed 30/380 bar for 5/10 min. Dropped 0.75 bar/10 min. Verified no pressure under XMT cap and removed same." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.0 hours. Operational details: Lowered the assembled XO, pump-in sub and short riser section through the rotary with tugger from drill floor and connected it to XMT. Installed BOP's with dual placed on top of tripple BOP." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Built scaffolding around BOP's to enabling handling of riser above BOP's." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Installed riser sections to rig floor." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 3.5 hours. Operational details: Opened SV. Attempted to pressure test riser sections and BOP's without sucess. Identified leak in FMC drain valve. Bled off pressure. Closed SV. Attempted to rectify the leaking valve without sucess." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.0 hours. Operational details: Built grease injection head, with cable head already installed and one lubricator section on rig floor. PU grease injection head and one lubricator section using tugger. Connected two more lubricator sections. Installed sheave wheels. Meanwhile drained riser and installed new FMC drain valve." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: PU and MU WL toolstring for pulling NPR plug and installed in lubricator. Connected lubricator at in-situ sub. Opened SV partly and flushed and filled lubricator with packer fluid using cement unit through KWV. Attempted to pressure test wireline rig-up. Observed leak in lubricator XO below tool catcher. Meanwhile transfered operation of HMV and TRSCSSV to pump skid in moonpool. Production operator was present during the transfer." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 0.8 hours. Operational details: BO lubricator and toostring. Changed leaking o-ring in XO. MU toolstring and re-connected lubricator." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Opened SV partly and flushed and filled lubricator with packer fluid using cement unit through KWV. Pressure tested wireline rig-up 30/185 bar for 5/10 min against HMV. Dropped 0.75 bar/10 min. Filled lubricator with 700 ltrs. Bled off pressure in lubricator/rig-up to cmt unit. Closed SV. Pressured up and opened HMV and TRSCSSV using WL pump in moonpool. Observed for leak on well head for 10 min. No leak observed. Opened SV." "On 2008-04-18, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Started RIH WL toolstring for pulling NPR plug. Production shut down at 23:57 and had shut down WL unit. Re-powered up WL unit." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: RIH WL toolstring for pulling NPR plug from surface to TRSCSSV at 496 m MDRT. Found that TRSCSSV was closed. Decided not to wait for cmt unit - production needed to equalize and open TRSCSSV on F-12 to re-start production. Hooked up pump on rig floor to needle valve on lubricator to equalize and open TRSCSSV in F-4. Ran through TRSCSSV at 496 m MDRT and verified that it was fully open." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Continued RIH WL toolstring for pulling NPR plug to 2600 m MDRT using running procedures for new cables. Running speed 40 m/min. Did not bleed off pressure while RIH and had 11-12 bar in well at 2600 m. Up weight 710 kg / Hanging weight 530 kg / RIH weight 422 kg." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: RIH and latched GS pulling tool into NPR plug at 2649.7 m. Jared down to equalize ports in the plug. Waited 15 min for pressure across plug to equalize. Pressure dropped to 10 bar. Bleed off pressure. Released NPR plug by jaring up once. Got 150 kg increase in string weight. Waited 30 min to allow elements to retract." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH with NPR plug. Observed that weight dropped back to up weight while POOH. RIH and latched GS pulling tool into NPR plug at 2649.7 m. Pressured up well to 10 bar. Jarred down to equalize ports in the plug. Waited 15 min for pressure across plug to equalize. No pressure drop observed. Released NPR plug by jaring up 105 hits. Adjusted stress point on cable after 60 hits with jar. Got approx 300 kg increase in string weight. Bleed off pressure. Waited 30 min to allow elements to retract." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: POOH with NPR plug on 7/32 cable, worked through TRSCSSV at 496 m with 200 kg overpull. Closed SV using 42 turns and closed HMV. Bled off pressure in XMT, riser and lubricator to closed drain." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: RD lubricator and cut wireline as per Seawell instructions. LD and inspected BHA and NPR plug. Plug had only small rift on rubber element." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.2 hours. Operational details: Held tool box meeting. Attempted to increase TRSCSSV CL pressure to 570 bar with Seawell pump without sucess. Max pressure of 540 bar with Seawell pump. RU Vetco pump to pressure up CL to 570 bar." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Lined up to test 7' tubing/liner to 380 bar through KWV with cmt pump. Opened LTV1 and LTV2. Pressured up well to test 7' tubing/liner to 35/380 bar for 5/10 min against EZSV plug at 3448 m MDRT. Pumped 1195 ltrs and bled back 1190 ltrs. Dropped 1.6 bar/10 min. Closed HMV. Adjusted TRSCSSV CL pressure to 520 bar." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Installed Check Valve in test line to cmt unit. Performed line test from cmt unit against KWV to 185 bar/10 min. Dropped 0.9 bar/10 min. Bled down to 10 bar on cmt unit to inflow test Check Valve. Bled down pressure between KWV and Check Valve to closed drain. Meanwhile RU scaffolding and lubricator to grease head." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.8 hours. Operational details: RU additional lubricator sections needed for perforation runs. Lifted riser sections to rig floor. Modified scaffolding to a higher level to be able to assemble lubricator. RU to run 7/16' electric line. Prepared grease injection head. MU cable head with PGGT." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Installed cable head and PGGT with bottom nose in riser. Connected WL riser at in-situ sub. Confirmed correct line up from cmt unit. Opened SV and KWV on XMT. Filled up riser and leak tested WL rigup to 30/185 bar for 5/10 min with cmt pump against HMV. Dropped 0.6 bar/10 min. Bled off pressure to closed drain. Closed SV." "On 2008-04-19, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Drained lubricator. Broke riser at in-situ sub and LD toolstring. Cleared drill floor. Installed nitrogen rack and regulator on drill floor." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 2.2 hours. Operational details: Discussed method for PU and MU perforation guns due to uncertified lifting cap." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held tool box meeting prior to PU and MU gun sections." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Checked GR/CCL on rig floor. Shut down power to Schlumberger unit to follow procedure for MU perforation guns. Closed off rig floor, WH and XMT. Made PA announcement." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.8 hours. Operational details: PU gun sections from cantiliver onto HTS with crane. Connected toolstring and swivel to gun and lifted guns into riser using both tugger and electric line with gooseneck. Connected and hung off all three gun sections in C-plate." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.8 hours. Operational details: MU firing head, PGGT and new swiwel to guns hung off in riser. Connected upper toolstring to guns hanging in riser and armed guns. PU tension on toolstring and took off C-plate." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3442m. The activity was categorized as 'workover -- wire line' and lasted for 3.8 hours. Operational details: Opened HMV and observed 2 bar WHP. Verified TRSCSSV was open. Opened SV and RIH with 4.5' TCP guns on 7/16' electric line from surface to 3442 m MD. Up weight 2850 kg / Running weight 1500 kg." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3426m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Bled 50 bar WHP down to zero through closed drain. Correlated guns to shooting depth using GR. Hanging weight 2570 kg. Fired guns and perforated interval #1 from 3408.5 m to 3422.0 m MD. Positiv confirmation that guns had fired, but observed no increase in WHP." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH and logged GR/CCL to above production packer. POOH with perforation guns to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.0 hours. Operational details: Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum. Broke lubricator at in-situ sub. BO and LD guns using sertified lifting sub. Observed that all shots had fired." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: PU gun sections from cantiliver onto HTS with crane. MU lifting sub and lifted guns into riser. Connected and hung off all three gun sections in C-plate." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Built and tested new cable head. Checked CCL on rig floor. Shut down power to Schlumberger unit according to procedure for MU perforation gun." "On 2008-04-20, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: MU firing head, CAL-B and new swiwel to guns hung off in riser. Connected upper toolstring to guns hanging in riser and armed guns." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Continued connecting upper toolstring to guns hanging in riser and armed guns. PU tension on toolstring and took off C-plate." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened SV." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3300m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: RIH with 4.5' TCP guns on 7/16' electric line from surface to 3300 m MD. Meanwhile worked on synergi report for derrick, performed general maintenace and prepared BOP for pressure test." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3390m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Correlated depth to 2 m pup-joint in 7' liner at 3228.38-3230.42 m tally depth / 3229.5 -3231.5 m WL dept correlated with GR on reservoar log using CCL." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3390m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: RIH with guns to shooting depth. No WHP. Up weight 2985 kg / Running weight 1540 kg. Hanging weight 2330 kg. Fired guns and perforated interval #2 from 3395.0 m to 3408.5 m MD. No obvious indication that guns has fired, but observed short circuit in string and CCL stopped working. Observed no increase in WHP. PU weight increased with 100 kg (3100 kg)." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 1800m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: POOH with perforation guns from 3390 m to 1800 m MD." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: POOH with perforation guns from 1800 m to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH. Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum. Broke lubricator at in-situ sub. Confirmed that guns had not fired." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 5.2 hours. Operational details: Disarmed guns and removed firing head. Found leak in rope socket/cable head which caused short circuit in toolstring. Built and tested new cable head. Checked CCL on rig floor. Shut down power to Schlumberger unit according to procedure for MU perforation gun." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: MU firing head, CAL-B and new swiwel to guns hung off in riser. Connected upper toolstring to guns hanging in riser and armed guns. PU tension on toolstring and took off C-plate. Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened SV." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 701m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: RIH with 4.5' TCP guns on 7/16' electric line from surface to 701 m MD." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 360m. The activity was categorized as 'interruption -- rig up/down' and lasted for 0.8 hours. Operational details: POOH with perforation guns from 701 m to 360 m MD due to weak CCL signal." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3408m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.8 hours. Operational details: Schlumberger discussed with town and confirmed that CCL was ok. RIH with 4.5' TCP guns on 7/16' electric line from 360 m to 3408 m MD." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3390m. The activity was categorized as 'interruption -- rig up/down' and lasted for 0.8 hours. Operational details: Correlated depth to 2 m pup-joint in 7' liner at 3228.38-3230.42 m tally depth / 3229.5 -3231.5 m WL dept correlated with GR on reservoar log using CCL. RIH with guns to shooting depth. No WHP. Fired guns and perforated interval #2 from 3395.0 m to 3408.5 m MD. Positiv indication that guns fired." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 2.2 hours. Operational details: POOH with perforation guns from 3390 m to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH. Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum. Broke lubricator at in-situ sub. Confirmed that guns had fired." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Connected lubricator and tested in-situ sub to 30/185 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened KWV. Pumped /bullheaded 3 m3 100% MEG at 180 lpm and 8 bar into well with cmt pump to provide cusion above closed TRSCSSV. Displaced MEG to above TRSCSSV by chasing it with 5.5 m3 packer fluid at 180 lpm and 8-20 bar. WHP started to increase after approx. 3 m3 packer fluid pumped." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Pumped 300 ltrs 100% MEG and displaced line with 500 ltrs packer fluid to fill XMT cross with 100% MEG. Closed TRSCSSV and HMV. Leak tested XMT cross to 123 bar / 10 min against closed HMV. Dropped 1.1 bar / 10 min. Bled off pressure to zero bar. Closed KWV." "On 2008-04-21, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Broke lubricator at in-situ sub. BO and LD guns using certified lifting sub." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: BO and LD guns using certified lifting sub. Observed that all shots had fired." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: RD lubricatoor on rig floor. Disconnected and pulled riser sections above BOP to rig floor." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Opened HMV and confirmed 0 WHP below. Closed HMV and opened KWV. Leak tested XMT cross to 123 bar / 10 min against closed HMV. Dropped 0.6 bar / 10 min. Bled off pressure to zero bar. Closed KWV." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Held tool box meeting. RD hydraulic BOP hoses. Disconnected WL BOP's and transfered to overhead crane in moonpool. Transported BOP's to main deck. Dismantled scaffolding around BOP's." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Installed tree cap and tested same 35/380 bar for 5/10 min against closed SV using Seawell test pump and 100% MEG. Bled off pressure." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: RD HP line from XMT KWV to cmt unit. Installed 1502 weco blind cap outside KWV and opened KWV. Leak tested KWV cap to 35/380 bar for 5/10 min aginst closed SV using Seawell test pump and 100% MEG." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Transfered operation of HMV and TRSCSSV to platform system/production. Filled in and signed 'Well handover document' and handed over well from Volve D&W to Mærsk Production at 09:00. Meanwhile RD scaffolding on rig floor and cleared rig floor of excess equipment." "On 2008-04-22, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Removed scaffolding around moonpool hatch and installed hatch. ****************END OF OPERATIONS****************" "On 2010-09-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 6.0 hours. Operational details: Well handed over from production department. Skidded rig in position. Changed to workover hatch. Meanwhile held pre job meeting with involved personnel." "On 2010-09-23, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Held tool box meeting on rig floor. Leak tested XMT cross to 20/100 bar for 5/10 min." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Installed chiksan manifold on TKV and leak tested same to 20/100 bar for 5/10 min." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Removed XMT top cap and installed lower riser and BOP. Leak tested lower riser/BOP connections and function tested BOP. Lowered down upper riser from rig floor and stabbed riser onto BOP. Meanwhile checked and tested RST toolstring on surface." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Held tool box talk and lifted up lubricator and GIH in elevator. Started to install toolstring into lubricator." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Continued installing toolstring into lubricator." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 1.5 hours. Operational details: Waited due to broken bolt in the wheel for KWV. Mechanic attempted to chang bolt without success and found a temporary solution." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Leak tested rig up. 20/100 bar for 5/10 min. Opened well. WHP = 7 bar." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 498m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH with BHA#1, RST. Stopped in DHSV at 498 m." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 498m. The activity was categorized as 'workover -- wait' and lasted for 0.5 hours. Operational details: Lined up AWS pump, pumped MEG into well and equalized DHSV at 39 bar." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Continued RIH with BHA#2, RST to 3420 m." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Ran correlation passes. Adjusted the depth according to reference log." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3230m. The activity was categorized as 'workover -- wire line' and lasted for 7.2 hours. Operational details: Logged RST-D in IC mode from 3390 to 3230 m at 0.5 m/min." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3400m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3400 m." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3230m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Logged RST in Sigma mode from 3390 to 3230 m at 4,5 m/min." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3400m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH to 3400 m." "On 2010-09-24, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3370m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Logged RST-D in IC mode from 3390 to 3370 m at 0.5 m/min." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3260m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Continued logging RST-D in IC mode from 3370 to 3260 m at 0.5 m/min." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3230m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Continued logging RST-D in IC mode from 3260 to 3230 m at 0.5 m/min." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: POOH with BHA #1." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: OOH. WHP 37 bar. Closed well and inflow tested HMV. Bled off and flushed lubricator with N2. Held toolbox meeting." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: LD RST toolstring and inspected same." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Closed BOP. Flushed riser with N2 through KWV to blow down." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Closed DHSV and bled down to 8 bar. Inflow tested DHSV. Bled off pressure above and closed well. Lined up and leak tested XMT cross." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Held toolbox meeting and LD lubricator onto cat walk machine. Lifted upper riser section to rig floor with top drive. Lifted BOP away in moon pool. RD lower riser." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Removed chiksan manifold on KWV and installed end cap. Installed XMT top cap. Leak tested KWV end cap and XMT top cap to 20/345 bar for 5/10 min. Disconnected local control panel for HMV and DHSV. Handed well over to Production department." "On 2010-09-25, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Disassambled riser and lubricator and lifted out riser sections from rig floor." "On 2010-09-26, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 6.0 hours. Operational details: Cleared rig floor off remaining WL equipment.Tidied and cleaned rig floor. Skidded rig in parking position. Prepared and packed WL equipment for demobilization. ---------------------------- END OF OPERATION --------------------------------------------" "On 2012-09-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Received WL equipment from boat." "On 2012-09-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Removed containers, tanks, equipment and prepared pipe deck area for spotting wireline equipment." "On 2012-09-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Started to spot WL equipment on pipe deck." "On 2012-09-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Leak tested BOP on stump. Started to prepare WL equipment." "On 2012-09-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Held Mearsk Toolbox Talk together with Maersk personnel prior to build lubricator. Held AWS check card meeting prior to thread the cable through GIH and toolcatcher." "On 2012-09-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.7 hours. Operational details: Lifted and spotted Smart skid in front of winch. Lifted toolcatcher and GIH to rig floor. Threaded the cable through GIH and tool catcher, prior to build cable head. Built lubricator with fork lift on main deck." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Waited on Mearsk electrician, prior to hook up all wireline units. Electrician busy with other jobs. Meanwhile lifted BOP down to BOP deck through hatch on drill floor and prepared wireline equipment." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.0 hours. Operational details: Waited on Mearsk electrician, prior to hook up all wireline units. Electrician busy with other jobs. Meanwhile prepared wireline equipment." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Hooked up wireline units to power and F&G." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Assembled lubricator and riser on rig floor." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Prepared wireline equipment. Meanwhile built cable head." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.0 hours. Operational details: Waited for Production Department to prepare well for handover. Meanwhile built cable head and megged same. Tried to connect logging unit to internet, no success." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Waited for Production Department to prepare well for handover. Meanwhile held start up meeting with night crew." "On 2012-09-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: Waited for Production Department to prepare well for handover. Meanwhile tested counter system and RST tool." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Waited for Production Department to prepare well for handover. Meanwhile tested RST tool." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.5 hours. Operational details: Waited for Production Department to prepare well for handover. Meanwhile tested RST tool." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Well handed over from production department." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held DOP#1 meeting prior to R/U on well." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Leak tested XMT cross to 20/120 bar for 5/10 min. Meanwhile prepared to install lower riser and BOP." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Held brief prior to install lower riser and BOP." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Removed XMT top cap and installed lower riser and BOP. Leak tested lower riser/BOP connections to 20/120 bar for 5/10 min." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Lowered down lower lubricator from rig floor and stabbed lubricator onto BOP." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held brief prior to install toolstring into lubricator." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Installed toolstring into lubricator." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held brief prior to lift up lubricator and GIH in elevator." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Connected hoses and lifted up lubricator and GIH in elevator. Connected toolstring and stabbed upper lubricator unto lower lubricator." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Held DOP#2 meeting prior to RIH with RST toolstring." "On 2012-09-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Prepared to leak test R/U." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Leak tested R/U to 20/120 bar for 5/10 min. Opened well. WHP = 42 bar." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held well controll drill prior to RIH." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 556m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: RIH with BHA#1, RST to 556 m." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 556m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Performed test of RST according to Schlumberger procedure." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Continued RIH with BHA#1, RST to 3420 m." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Ran correlation passes. Adjusted the depth according to reference log." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3210m. The activity was categorized as 'workover -- wire line' and lasted for 1.1 hours. Operational details: Logged RST-D in Sigma mode from 3400 to 3210 m at 4,5 m/min." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: RIH to 3420 m." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3215m. The activity was categorized as 'workover -- wire line' and lasted for 6.8 hours. Operational details: Logged RST-D in IC mode pass#1 from 3410 to 3215 m at 0,5 m/min." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: RIH to 3420 m." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3215m. The activity was categorized as 'workover -- wire line' and lasted for 8.0 hours. Operational details: Logged RST-D in IC mode pass#2 from 3410 to 3215 m at 0,5 m/min." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3420 m." "On 2012-09-14, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3380m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Logged RST-D in IC mode pass#3 from 3410 to 3380 m at 0,5 m/min." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3180m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Logged RST-D in IC mode pass#3 from 3380 to 3250 m at 0,5 m/min." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 3220m. The activity was categorized as 'workover -- wire line' and lasted for 1.7 hours. Operational details: Continued logging RST-D in IC mode pass#3 from 3250 to 3220 m at 0,5 m/min." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: POOH from 3220 m to surface. WHP:42 bar." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.5 hours. Operational details: OOH. Closed in SWAB and HMV. Inflow tested same. Opened HMV and inflow tested DHSV." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: L/D upper lubricator on drill floor and removed BHA#1, RST-D logging tool." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Performed brief prior to rig down." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Lifted lower lubricator to rig floor with top drive. Lifted BOP away in moon pool. R/D lower riser." "On 2012-09-15, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.8 hours. Operational details: Removed chiksan manifold on KWV and installed end cap. Installed XMT top cap. Leak tested KWV end cap and XMT top cap to 20/345 bar for 5/10 min. Disconnected local panal for HMV and DHSV. Handed well over to production department. ---------------------------------------- END OF OPERATION-------------------------------------------------" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Reporting continued from F-99. Continued to skid cantilever to F-04 9m inboard/1.25m port. Continued work with Aft PRS" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Installed covers to skidding system. Meanwhile held TBT for connecting HP hose to F-04 and for removal of well head cover/installation of split cover" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Connected HP hose to F-04. Meanwhile tested aft PRS. Prepared subs for pressure testing" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Performed line test down to XMT. Performed test of XMT cross 20/345bar for 5/10min. Good test" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to remove moonpool hatches" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed hatches and installed split hatch" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Adjusted scaffolding around Xmas tree. Prepared lines and bled off A and B annulus to MGS. Worked to fill A and B annulus with sea water. Bled off pressure and removed Tree cap from Xmas tree w/ rigfloor winch" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Hooked up hydraulic pump for local control of DHSV an HMV. Meanwhile worked to fill A and B annulus with sea water, carried out TBT for R/U cement head" "On 2016-10-01, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Worked to P/U cement head in moonpool using overhead crane and transfered to TDS lifting chains" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Worked to P/U cement head in moonpool using overhead crane and transfered to TDS lifting chains" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: M/U cement head to the Xmas tree, installed split hatch in moonpool" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Built scaffolding around cement head in moonpool" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pressure test cement head" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Confirmed line up, flushed and pressure tested cement head and bleed off manifold to 20/345 bar for 5/10 min" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting before bullheading operation" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lined up to pump into the well. Opened HMV. Wellhead pressure went up to 20 bar. Bled off pressure to MGS. Pressured up DHSV control line to 520bar. Pressured up above DHSV to equalize pressure. Observed indecation of DHSV openning on hydraulic pump pressure gauge." "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pumped 10m3 of wash pill, 1100 l/min - 134bar" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Bullheaded sea water into the well, 1300 l/min - 143 bar, totally pumped 140m3. Meanwhile carried out TBT for cement job" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Lined up valves on the cement head, released bottom dart, mixed and pumped 13.6m3 1,90SG cement, 600l/min. Pressure 130 bar, decreasing to 90bar, indicating cement moving down in the tubing. Displaced lines w/ 0,9m3 of Hi-vis pill. Released top dart. Pumped 12,2m3 of Hi-vis (totally pumped 13,1m3 of Hi-vis). Displaced w/ 37,7m3 of sea water at initial rate of 1000lpm. Increased pumping rate to 1300l/min - 101bar. Reduced pumping rate in the end of displacement to 700l/min - 83bar. Switched to contamination pill. Observed rapid increase in pressure while pumping contamination pill indicating cement plugging into perforations. Shut down after having pumped 3,5m3 contamination pill, 111 bar and monitored WH pressure decline. Recorded final stabilized squeeze pressure of 60bar. Closed swab valve. Verified volumes pumped by checking volumes left in the pits and silos. Theoretical top of cement 2755mMD. DHSV was cycled 3 times after 30m3 of sea water displacement was pumped" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Flushed manifolds after cement job. Worked aloft in derrick to repair crown grease system. Lined up and prepare to pressure test BOP. Meanwhile WOC" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed BOP test No1 20/345 bar 5/10 minutes. Cycleed HMV and MMV. Meanwhile WOC" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lined up for BOP test No2, flushed 0.5m3 through kill and choke lines" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Performed BOP test No2 20/345 bar 5/10 minutes. Cycled HMV and MMV. Meanwhile pumped out dirty side of skimmer tank to mill tank, WOC" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Lined up and performed BOP test No3 20/345 bar 5/10 minutes. Continued to clear out dirty side of skimmer tank, transfered to mud pits 7.5m3. Lined up to bleed off pressure from XMT 110bar down to 62bar. Meanwhile WOC" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Opened all low torque valves on cement head and pressure tested rig up against SV to 310 bar/10 minutes. Meanwhile WOC" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Closed HMV , bled off pressure above HMV from 72bar to 0. Opened SV, pressured up to 72bar to equalize, opened HMV. Pressured up well against cement plug with cement pump to 310bar/10min. Pumped 620liters. Good pressure test." "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Carried out inflow test of cement plug. Bled down pressure in tubing to 10 bar. Monitored pressure pressure for 30 min. Pressure increased 3.6 bar with clear decreasing trend towards the end. Good inflow test" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Carried out inflow test of DHSV. Equalized pressure and opened swab valve, applied 310 bar to tubing. 770l pumped. Closed DHSV. Bled off pressure in tubing above DHSV to 240 bar. Monitored pressure above DHSV for 30 min for 70bar LP inflow test. Pressure increased 1.5bar in 30 min with decreasing trend towards the end. Good LP inflow test. Bled down pressure in tubing above DHSV to 10bar. 110l bled off. Monitored pressure above DHSV for 30 min for 300bar HP inflow test. Pressure increased 2,4bar in 30 min with decreasing trend towards the end. Good HP inflow test. Equalized pressure above DHSV, pressured up control line to DHSV to 520bar to open DHSV. Bled off tubing pressure to 20bar. 710l bled off. Closed DHSV. Bled off remaining pressure from Xmas tree. Meanwhile performed TBT to R/D cement head" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Closed SV. R/D cement head. Removed hydraulic control hoses to HMV and DHSV. Broke off bleed off manifold from kill wing side" "On 2016-10-02, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Worked to installed BPV plug for drop protection and Xmas tree lifting cap. Meanwhile performed BOP test No4" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued to install BPV plug for drop protection and Xmas tree lifting cap. Meanwhile worked to perform BOP test No5" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Remove scaffolding from around Xmas tree and R/D electric and hydraulic lines from Xmas tree. Meanwhile performed pre-job meeting to N/D Xmas tree, pressure tested BOP test No5" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed hatches and beam between slots. Meanwhile worked to pressure test BOP test No6, 7" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed master bushing and outer ring. Lowered diverter chains on TDS bails to wellhead and attached to X-tree. Meanwhile pressure tested BOP test No7" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to lift Xmas tree" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Took weight as per lifting plan and removed Grayloc clamp. Lifted X-tree to moonpool. Transfered load to gantry crane in moonpool. Attached lifting arrangement from TDS to Spacer spool" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Released NT-2 connector on wellhead, had difficulties to release 2x tight bolts. Meanwhile prepared HP riser on rig floor" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Cut control lines, installed communication collar and dart on BPV, cleaned up seal area. Meanwhile P/U riser from HTS" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed covers in moonpool using rigfloor winch" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and RIH HP riser and M/U NT-2 connector" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Removed scaffolding from test stump and built scaffolding around HP Riser. Performed checks prior to skid BOP to well center. Meanwhile worked to M/U TDS test assembly" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to move BOP to well center" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Skidded BOP to well center and landed off on HP riser. Meanwhile pressure tested kelly hose to 20/345 bar, 5/10 min" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to M/U NT-2 connector" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: M/U NT-2 connector. Meanwhile pressure tested upper/lower IBOPs and 2x FOSVs to 20/345 bar, 5/10 min" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to connect tension cylinders" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: R/U tension system" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to handle slick joint" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed master bushing, RIH with Slick joint and M/U same, measured RKB to top of Annular = 5.78m" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to handle diverter" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U and RIH w/ diverter and landed off. Continued M/U slick joint. Meanwhile removed chains from bails and connected overshot hose. Energized overshot, lined up and filled hole with 3m3. No leaks observed" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up cement unit through kill HCR, closed BSRs. Applied 20 bar to kill HCR valve to confirm line up" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: With slick joint made up, fine tuned tension cylinders for equal pull" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed connection test to 20/345 bar 5/10 min, good test" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Finished to M/U slick joints, cleaned and cleared rig floor" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed handling equipment to 3.5in DP" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to retrieve dart and BPV" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Retrieved dart from BPV" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Retrieved BPV" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/B 3.5in DP, L/D retrieval tool" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed handling gear, prepared for running THRT" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U casing tong" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U casing tong" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to run w/ THRT and landing string" "On 2016-10-03, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and RIH with tubing hanger running tool (THRT)." "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued to P/U and M/U tubingTHRT and landing string. POOH, installed control lines and inspected THRT. RIH and landed off THRT on TH. Observed top box of landing string is too high for casing tong to be able to M/U swedge." "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to rearrange landing string to be able to M/U swedge w/ casing tong. Started to position upper pup joint of landing string for casing tong to break off. Observed hydraulic oil leak from elevator" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Identified faulty hydraulic hose inside of the elevator and changed same" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Broke top 6m pup from landing string. M/U swedge using aft PRS and casing tong. Realized that it is not possible to break swedge while connected to TH with THRT. Broke off swedge using aft PRS and casing tong. Located 4m tubing joint (3m + 1m pups) on the pipe deck. M/U same to landing string, M/U 1m pup joint to landing string. Achieved sufficient stick up to be able to M/U swedge" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Attempted to engage THRT to TH. No success, POOH, checked THRT, observed shear pins sheared prematurely. Repaired THRT" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH and landed off THRT, engaged tool and confirmed w/ 2t overpull. Applied pressure to shear pin and then rotated string 8x turns CCW into communication collar" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Connected cement hose and LT valve, flushed hose. Pressure tested same to 100 bar. Lined up pumps through cement hose. Applied pressure of 520bar to DHSV control lines. Pressured up well above DHSV, observed DHSV equalized and opened at 100 bar pressure. No indications of gas below DHSV/in the well observed. Bled off pressure from the well through the cement hose to MGS to 0. Closed DHSV. Verified no pressure in the A-annulus" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Broke off swedge" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Released TH and and pulled 180t on hook load. String stretch of 0,75m" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U WL equipment" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U wireline equipment" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2616m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: RIH w/ cutter BHA, run #9 from surface 2616 m. Average running speed 20 m/min." "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2621m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Correlated across interval 2616 - 2638 . Positioned cutter at 2621 m . Performed cut. Observed backflow from pipe after tubing was cut" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: POOH from 2621 m to surface. Average pulling speed 22 m/min. Backflow at rotary gradually decreased and eventually stopped" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D wireline equipment" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed flowcheck. Static" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2600m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: POOH w/ tubing and tubing hanger on landing string. Spooled control line. L/D landing string and TH on deck" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2600m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed casing slips and control line spooler" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2600m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull and L/D 7in tubing" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2595m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D 3x pup joints" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2573m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled and L/D 2x joints of tubing" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2573m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull and L/D 7in tubing w/ new crew" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2573m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Checked red zone barriers and equipment" "On 2016-10-04, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2109m. The activity was categorized as 'plug abandon -- other' and lasted for 4.5 hours. Operational details: Pull and L/D 7in tubing from 2573m to 2109m, spooled control line. Pulled and L/D DHSV assembly. Average pulling speed 8,5 joints/hour. Totally pulled 39joints and DHSV assy" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2049m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled and L/D the remaining 5x joints of 7in tubing. Average pulling speed 7joints/hour. Totally pulled 45x joints and DHSV assy" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2049m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to M/U swedge" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2049m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U swedge assembly w/ casing tong" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2049m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Removed control line drum. Moved casing tong. Broke off swedge from FOSV. Install 5,5in inserts in BX elevator. M/U 1x std of 5,5in DP. Removed casing slips and installed DP slips. Cleared rig floor" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2049m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: RIH w/ 7in tubing on 5,5in DP from 2049m to 2291. Average RIH speed 485m/hour" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2291m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Filled pipe" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2616m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: RIH w/ 7in tubing on 5,5in DP from 2291m to 2616m. Average RIH speed 650 m/hour" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2616m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to circulating well to sea water" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2616m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Started to circulate well to sea water. Staged up pumps to 3000 l/min - 78bar. Observed dirty fluid in returns. OIW reading is above 100ppm. No gas. After 50m3 pumped pulled 3m above combination wiper plug. Continued circulating. Shakers overflowed, reduced the rate to 2200l/min - 56bar. Circulated additional 112 m3. Observed clear returns after total of 162 m3 pumped. OIW content less than 30 ppm. Stopped pumps. Installed pump in sub w/ LT valve." "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2614m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: R/B 1x stand. Installed side entry sub assembly and connected cement hose, spaced out to 2614m bottom of tubing string" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2614m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Lined up/prepared to pump wash pill" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2614m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to place pump balance cement plug" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2614m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 20m3 wash pill with mud pumps, 2700l/min - 79bar. Applied 20 bar behind IBOP, verified line up" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2416m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Balanced cement plug (2616 m - 2416 m ): Mixed and pumped 9,4 m3 of 1,9 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 2900 l of drill water. Zeroed volume counters. Displaced the cement with 37 m3 (1670 strokes) of SW, 2900 l/min/ 51 bar. Pulled out of cement to 2416m at 4 min/stand. Theoretical TOC 2416 m MD." "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2372m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Installed sponge ball. Pumped 10m3 hi-vis at 2400l/min / 43 bar. Circulated out cement at max of 3400 l/min/ 116 bar. Diverted returns overboard. L/D pup joint and R/B 1x stand to 2372m. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2372m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to wash BOP w/ jetting tool. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2372m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Installed closed FOSV and BOP wash tool, made 10x passes in BOP and well head area at 1500 LPM / 12 bar, operated rams and annular once. L/D BOP wash tool. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2372m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D DP. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2052m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Installed pipe deck rollers. POOH and L/D singles of 5,5in DP from 2372m to 2052m. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2052m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed DP slips and installed master bushing. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2052m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U casing tong. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2049m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: R/U casing tong and broke off swedge from top of tubing string. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2049m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: R/D casing tong. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2084m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U spear BHA, set in catch position and engaged into tubing string, RIH to 2084m. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2365m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: RIH w/ 5,5in DP from 2084m to 2365m. Average tripping speed 612 m/hour. Performed kick drill. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2365m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Performed maintenance on TDS. Cleared chiksans from wellhead. Worked on PMs on drilling equipment. Tested back up BX elevators, good test. Meanwhile WOC" "On 2016-10-05, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2365m. The activity was categorized as 'plug abandon -- other' and lasted for 5.0 hours. Operational details: Cleaned in moonpool. Worked to service both PRSs and TDS. Installed drill pipe slips. Meanwhile WOC" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2436m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Initiated circulation and RIH to tag cement. Down weight 129t. Slowly washed down from theoretical TOC of 2416m to 2426m. 500l/min - 11bar. No indication of cement, stable pressure. Continued RIH. Observed increase in pressure to 13-14bar and no change of weight indicating poor cement. Stopped RIH at 2436m, 20m below theoretical TOC. Picked up string 10m and circulated well over shackers at max 2000l/min - 100bar. Shackers plugged with cement returns. Diverted returns overboard. Continued circulated until no cement observed in returns. Totally circulated 108m3. Meanwhile WOC" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2405m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Waited for cement, total of 2 hours from 1st tagging attempt" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2438m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Initiated circulation and RIH to tag cement. Down weight 126t. Slowly washed down from 2436m, 500l/min - 10bar, pressure dropped to 8 bar after reaching 2438m. Tagged TOC w/ 10t. Confirmed TOC at 2438m (22m below theoretical TOC)" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 2438m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Released spear from tubing string. Pulled string 2m up, confirmed spear released, up weight of 82t. Top of tubing 389m" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 389m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D 5.5in DP. Meanwhile performed flowcheck. Stable" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: POOH w/ spear and L/D 5.5in DP" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D spear BHA" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed DP slips, installed master bushing" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: L/D spear BHA" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed power rollers. Cleaned and cleared rig floor" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U wash tool. RIH from surface to 20.5 m. Jetted wellhead w/ 2200 l/min, 10 rpm, moved string 1m up/down. POOH, L/D jetting tool" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U MS-T seal retrieval tool" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: P/U and M/U MS-T seal retrieval tool and tested same RIH to 20.5m and engaged MS-T seal retrieval tool. Pulled seal free with 80t overpull POOH from 20,5m and L/D MS-T seal and retrieval tool" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U cutter BHA" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U and RIH cutter BHA to 9,5m" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 123m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ cutter BHA, positioned knives at 123m" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 123m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: M/U TDS, took parameters. Cut 10 3/4in surface casing tieback at 123m, 400 l/min - 50bar, 80 rpm, 2-10 kNm. Observed good indications of cut: pressure drop and reduction of torque" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flowchecked for 5min, stable. POOH to 9,5m" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D cutter BHA" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U casing tong" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/U casing tong on the rig floor" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 103m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ spear and engage in 10 3/4in surface casing hanger, pulled casing to surface" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 103m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull and L/D 10 3/4in casing" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 98m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Broke out pup joint and casing hanger, L/D same" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 98m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Changed BX Elevators to BX-4s and PDM head" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.8 hours. Operational details: POOH and L/D 10 3/4in caing tieback from 103m to surface" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: R/D casing tong and changed BX elevators" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to change saver sub to left hand one" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Placed 3m pup in rotary. Screwed in TDS and broke off saver sub. L/D pup with saver sub on top. RIH 1x stand with left hand DP. M/U left hand saver sub to stand, screwed in TDS and M/U to saver sub" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/B stand and P/U torque tool" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH w/ torque tool on LH drill pipe to 140m" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Washed profile area 1500l/min - 9bar. Released tieback adapter w/ 38kNm" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to change handling gear, L/D 5,5in LH DP" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed master bushing, installed DP slips. Changed PDM head" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 7m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/B 1x stand of LH DP, L/D 16x joints of LH DP" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/D torque tool" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D 4x singles of LH DP from the stand previously R/B" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed DP slips, installed master bushing" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to change saver sub back to right hand one" "On 2016-10-06, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Worked to change saver sub back to right hand one" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Worked to change saver sub back to the right hand one" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U spear BHA" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 128m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH w/ ITCO spear BHA" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Engaged spear in tieback adapter fish, pulled w/ 6t overpull. POOH w/ fish to surface" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/B spear BHA, L/D tieback adapter stump" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT to P/U perforation guns" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 2.5 hours. Operational details: M/U and RIH w/ perforation BHA to 148m bottom shot depth" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Closed UPR, opened choke. Confirmed line up. Filled string. Opened UPR, Broke off TDS and dropped 1 3/8 ball in string. M/U TDS. Closed UPR and opened choke. Fired guns with 160 l/min - 130 bar. Top shot at 145m, bottom shot at 148m. Continued to circulate w/ 160l/min" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Circulated 1000 lpm / 5 bar. Maximum gas reading 0,41 %." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Stopped pumps and closed choke. Monitored well. Unable to circulate on TT due to contaminated OBM mixed with water. Emptied both TTs and re-filled TTs with clean SW." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Opened UPR and choke Flowchecked well for 10 min, static." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 14m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: POOH w/ perforation BHA from 148 m to 14 m." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 14m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Changed to 4 1/2' inserts in BX-elevator." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: L/D perforation BHA." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT for cutting 10 3/4' casing" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed master bushing. Installed PS-21 slips." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U and M/U 10 3/4' cutter BHA." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 312m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ 10 3/4' cutter BHA on 5 1/2' DP from surface to 312 m." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 312m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: M/U TDS. Recorded up/down weight 76 / 71 ton. Filled DP. Initiated circulation 500 lpm / 73 bar, 50 rpm / 0 to 3 kNm." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 312m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cut 10 3/4' casing at 312 m, 400 lpm, 50 rpm. SPP dropped, good indication of cut." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 312m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Lined up to TT and performed flowcheck, well static." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH w/ 10 3/4' cutter BHA on 5 1/2' DP from 312 m to 9,5 m." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D cutter BHA." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT for drops inspection prior to milling 10 3/4' casing hanger." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Performed drops inspection of TDS, and both PRSs." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 72m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.2 hours. Operational details: M/U CH milling BHA" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: RIH w/ CH milling BHA on 5 1/2' DP from 72 m to 110 m. M/U TDS and continued RIH, tagged top of 10 3/4' CH at 139,9m. Pulled up and filled string." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.2 hours. Operational details: Milled ID in 10 3/4' CH to 12 1/4'. 100 rpm / 9-18 kNm, 2000 lpm / 10,8 bar, 4-5 ton WOB. Increased WOB to 8 - 10 ton after milling first 20 cm." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.2 hours. Operational details: Continued milling 10 3/4' CH, 100 rpm / 10 - 16 kNm, 2000 lpm / 11 bar, WOB 8 - 10 ton. Stalled out several times" "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Tagged top of 10 3/4' casing 1 m below 10 3/4' CH. Dressed off approximately 5 cm of top of 10 3/4' casing, 120 rpm / 5 - 10 kNm, 2000 lpm / 10 bar." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Circulated 2 x B/U w/ 3000 lpm / 22 bar. R/B 1 stand 5 1/2' DP." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 110m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Performed drops inspection of TDS. Meanwhile: Flowchecked well, static. Performed TBT for L/O milling BHA." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 72m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: POOH w/ CH milling BHA on 5 1/2' DP from 110 m to 72 m." "On 2016-10-07, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/B 8 1/4' DC. B/O and L/O CH milling BHA." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Cleaned and cleared drill floor" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with spear and retrieve 10 3/4' casing" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: M/U spear BHA" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 147m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: RIH w/ 10 3/4' spear in catch mode on 5 1/2' DP from surface to 147 m" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: POOH with 10 3/4' casing on 5 1/2' landing string from 147 m to surface." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Released spear at surface and R/B spear BHA" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for R/U casing handling equipment and pulling casing." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 3.0 hours. Operational details: L/D casing pup joint. Continued POOH with 10 3/4' casing from 170 m to surface. Average 10 joints/hr." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.2 hours. Operational details: R/D handling equipment." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for running 13 3/8' EZSV plug" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 24m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: P/U and M/U EZSV plug and RT. Installed centralizer on RT. L/D double 5 1/2' DP. P/U and M/U 3 pup joints for space out" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 306m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH w/ 13 3/8' EZSV plug from 24 m to 306 m." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 306m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U pump-in sub." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 306m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: M/U TDS and washed setting area with 560 lpm / 6 bar. Set 13 3/8' EZSV plug at 306m. Tagged EZSV plug with 10 ton." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 305m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Pumped 10 m3 wash pill followed by 10 m3 hi-vis pill at 2000 lpm / 9 bar. Circulated with clean SW until clean returns. Reduced to 900 lpm when hi-vis at shakers. Increased flow to 2440 lpm when clean SW in returns. Meanwhile: Flushed TTs." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 305m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for cement job" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 305m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Closed flow line and opened dump line. R/U cement hose to pump-in sub. Applied 20 bar behind FOSV and confirmed line-up. Leak tested surface lines to 100 bar / 3min. Balanced OH to surface cement plug in 13 3/8' casing (305 m - 205 m ): Pumped 10 m3 DW at 1000 lpm with cement unit. Mixed and pumped 7,8 m3 1,95sg cement slurry at 600 lpm. Displaced cement with 2 m3 DW at 1000 lpm with cement unit." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 305m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/D cement hose. B/O and L/O pump-in sub." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 160m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 305 m to 160 m." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 160m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed 2x sponge balls. Circulated BU, 2000 lpm." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 80m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 160 m to 80 m. M/U BOP jetting tool and FOSV." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 80m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Jetted BOP 8 x passes up/down, 1450 lpm, 50 rpm. Operated annular preventer and pipe rams. B/O and L/O BOP jetting tool and FOSV." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 80m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed master bushing." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH and L/D the EZSV RT." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: RIH with 3 std 8 1/4' DC. L/O 2 x singles to cantilever." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Performed TBT with ongoing crew. Performed manual tong training. L/O 7 joints 8 1/4' DC." "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O 10 3/4' spear BHA" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: L/O 3 joints 6 3/4' DC" "On 2016-10-08, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O 5 joints over-torqued 5 1/2' DP" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: L/O 13 joints 5 1/2' over-torqued DP" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: L/O 4 joints over-torqued 5 1/2' HWDP. Used manual tongs to break one of the connections." "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor. Changed handling equipment for pulling diverter." "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/D BOP" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: N/D diverter and pulled slickjoint." "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Load shifted weight from tension system to BOP carrier." "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Disconnected BOP tension system. Meanwhile: Disconnected BOP NT2 connector" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Skidded BOP over to test stump" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed scaffolding around HP-riser. Meanwhile: Performed TBT for pulling HP-riser" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled HP-riser to drill floor. Installed master bushing." "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/O HP-riser to HTS and installing hatches in moonpool" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O HP-riser to HTS" "On 2016-10-09, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Installed hatches in moonpool. Meanwhile: Cleaned and preserved slickjoint ******** END OF REPORT - CONTINUED REPORTING ON F-99 *********" "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: Waited on supply boat with equipment for pulling production riser Meanwhile: L/O 3 1/2' DP from set-back. Meanwhile: Performed PMs." "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: Waited on supply boat with equipment for pulling production riser Meanwhile: Canged handling equipment to handle 5 1/2' DP. L/O 5 1/2' DP from set-back." "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: Continued L/O 5 1/2' DP from set-back. Meanwhile: Removed remaining hoses and electrical cables from WH" "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/D diverter" "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U and attached lifting equipment to TDS and diverter. L/O diverter and secured same on main deck. Removed diverter lifting equipment from TDS. Meanwhile: Performed TBT for building scaffolding around BOP connector on test stump." "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Prepared 1502 hoses/chiksan at WH Built scaffolding around BOP." "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: N/U BOP NT2 connector on test stump. Prepared lifting equipment on moonpool hatch. Lifted multibowl NT2 connector to drill floor. Lifted PR cutter BHA to HTS" "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Continued N/U BOP NT2 connector on test stump" "On 2016-10-10, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed hatch in moonpool." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lowered NT2 connector for multibowl. M/U NT2 connector on multibowl." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed master bushing and removed box ring from rotary." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for handling PR cutter BHA" "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: P/U and M/U cutter BHA and RIH with same. P/U and M/U mutlibowl RT." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ BHA and M/U multibowl RT in WH. Took 20 ton OP to verify RT engaged in WH. M/U TDS Performed debrief after M/U BHA." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT for R/D tension cylinders on PR" "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Bled off pressure in PR tension cylinders, observed 35 ton increase on weight indicator" "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Prepared WH/tension ring for removal" "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for removing tension cylinders with ongoing crew" "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.2 hours. Operational details: Continued bleeding off tension cylinders. R/D tension cylinders, left the cylinders hanging from top mounting point. Secured tension cylinders. Meanwhile: Assisted crane with backload. Cleaned shaker pits." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed information meeting with all involved personnel for riser pulling operations." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: R/D boat collision stool and prepared to remove centralizers from centralizer deck. Connected 3 x weco 1502 hoses to WH outlets. Meanwhile: Assisted crane with backload. Continued cleaning shaker pits." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: Waited on supply boat for riser equipment Meanwhile: Performed housekeeping on cantilever. Removed pipes and equipment from cantilever to make space for riser joints. Assisted crane with backload. Continued cleaning shaker pits." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U riser handling equipment" "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: R/U tailing arm and saddle on HTS. Continued to clear cantilever. Installed beams on cantilever deck for L/O riser joints." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed information meeting with all involved personnel for riser pulling operations." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Continued to clear cantilever. Installed deck beams on cantilever." "On 2016-10-11, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Spotted riser handling equipment. Meanwhile: Cleared drill floor." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued spotting riser handling equipment. Meanwhile: Cleared drill floor." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for cutting the production riser and pulling the multibowl to drill floor." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Took 5 ton overpull. Staged up pump rate to 900 lpm, observed water leaking over the top of the multibowl" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Stopped pumping. Checked scribe line to confirm multibowl running tool still engaged to the multibowl." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Staged up pump rate to 2300 lpm / 87 bar. Continued pumping for approximately 15 min, lost overpull, good indication of cut. Observed multibowl/riser turned 1/4 turn clockwise at successful cut." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U slowly to confirm successful cut." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed hoses and valves from multibowl." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser and multibowl to drill floor. Removed master bushing and installed the big C-plate." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Disengaged multibowl RT by rotating elevator." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed small C-plate and false rotary." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: B/O and attempted to rack back multibowl RT. Unable to rack back due to too long assebly. Parked AFT PRS with multibowl RT out of the way." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Pulled inner string and R/B 2 x 5 1/2' DP stands. R/B cutter BHA" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U multibowl RT. Removed C-plate." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled up riser until first flange at centralizer deck. Cleaned flange for marine growth." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling and cutting riser" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled tensioner joint above drill floor. Cleaned flange for marine growth on WH deck." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed master bushing and elevator. Landed riser on elevator." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U cutting machine. Installed hole cover to collect swarf" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Cut tensioner joint" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Collected swarf. R/D cutting machine." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: L/O tensioner joint" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Removed running tool. Changed handling equipment. Installed cradle on HTS Cleared drill floor." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lifted riser. Removed master bushing" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled riser (lift #2). Cleaned flanges on WH deck" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed master bushing and elevator. Removed fairing and landed riser onto elevator" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine and hole cover. Cut riser" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Collected swarf. R/D cutting machine." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (lift #2)." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (lift #3)." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing. Pulled flange through rotary. Installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting maching and cut riser" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting maching. Collected swarf" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D riser joint (lift #3)" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser joint (lift #4). Pulled master bushing. Pulled flange through rotary, installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting maching and attempted cut riser. Knifes worn out and broken." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Changed knifes and continued cutting riser. Experienced knifes not cutting evenly due to ovality of riser." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued cutting riser. Meanwhile: Performed TBT with ongoing crew." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting maching. Collected swarf" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (lift #4)." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled riser (lift #5) Removed master bushing. Pulled flange through rotary, installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U cutting manchine and cut riser. Experienced knifes not cutting evenly due to ovality of riser." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting machine. Collected swarf" "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (lift #5)." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (lift #6). Removed master bushing. Pulled flange through rotary, installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine and cut riser." "On 2016-10-12, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting machine. Collected swarf." "On 2016-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (lift #6)." "On 2016-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lifted riser (lift #7). Removed master bushing. Pulled riser. Installed master bushing and hole cover in rotary." "On 2016-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint." "On 2016-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed hole covers and hatches." "On 2016-10-13, at Well NO 15/9-F-4, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed elevator to handle BHA. Meanwhile: Removed scaffolding in moonpool. ******* END OF REPORT *******" "On 2013-08-23, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 2620 m to 2632 m, controlled ROP 10 m/hr. WOB 5 - 12 tonne. 2000 l/min/ bar. 80 rpm / 8 - 12 kNm. Started bleeding in LCM premix, 4m3 per stand for drilling Ty Fm." "On 2013-08-23, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2673m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 8 1/2' hole through Ty Fm. from 2632 m to 2673 m, average ROP 20 m/hr. WOB 5 - 12 tonne. 2000 - 2400 l/min/ 143 - 170 bar, ECD: 1,34. 80 - 140 rpm / 11 - 22 kNm. Increased rpm after top stab out of casing shoe. Bleed in LCM premix as per plan to maintain particle concentration." "On 2013-08-23, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2771m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and oriented 8 1/2' hole through Ty Fm. from 2673 m to 2771 m maintaining constant drilling parameters and bleeding in LCM premix, average ROP: 28 m/h. WOB 5 - 12 tonne. 2400 l/min/ 170 - 175 bar. 140 rpm / 12 - 20 kNm. ECD 1,36 SG" "On 2013-08-23, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2857m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled and oriented 8 1/2' hole in Shetland Gp. from 2771 m to 2857 m, average ROP: 19 m/hr. WOB 5 - 12 tonne. 2400 l/min/ 175 bar. 140-160 rpm / 12 - 25 kNm. ECD: 1,37. Increased rpm to 160 to combat high stick slip." "On 2013-08-23, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2857m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR" "On 2013-08-23, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2892m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled and oriented 8 1/2' hole in Shetland Gp. from 2857 m to 2892 m, average ROP: 20 m/hr. WOB 10 - 12 tonne. 2400 l/min/ 175 bar. 160 rpm / 11 - 26 kNm. ECD 1,37. Added four sacks Baracarb 50/150 and Steelseal 100/400 per stand to maintain LCM background concentration." "On 2013-08-23, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3004m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and oriented 8 1/2' hole in Shetland Gp. from 2892 m to 3004 m, average ROP: 22 m/hr. WOB 10 - 14 tonne. 2400 l/min/ 175 - 178 bar. 160 rpm / 12 - 25 kNm. ECD 1,37 - 1,38 SG. Added four sacks Baracarb 50/150 and Steelseal 100/400 per stand to maintain LCM background concentration." "On 2013-08-24, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3004 m to 3070 m, average ROP: 22 m/h WOB 5 - 12 tonne. 2400 l/min/ 175 - 180 bar. 160 rpm / 15 - 22 kNm. ECD 1,38 SG. Started to increase MW from 1,28 SG to 1,32 SG." "On 2013-08-24, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3094m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled and oriented 8 1/2' hole from 3070 m to 3094 m, average ROP: 15 m/hr. WOB 5 - 8 tonne. 2400 l/min/ 183 bar. 160 rpm / 15 - 20 kNm. ECD 1,39 SG. Experienced problems in achieving required build rate, controlled ROP to 15 m/hr, set build force to 97%, reduced walk force. Increased MW from 1,28 SG to 1,32 SG. Maintained LCM background concentration" "On 2013-08-24, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3128m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and oriented 8 1/2' hole from 3094 m to 3128 m, average ROP: 9,7 m/hr. WOB 1 - 3 tonne. 2400 l/min/ 183 bar. 160 rpm / 12 - 17 kNm. ECD 1,40 SG. Controlled ROP to 10 m/hr to improve steering capability. MW in - out: 1,32 SG. Maintained LCM background concentration" "On 2013-08-24, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3317m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3128 m to 3317 m, average ROP: 17,2 m/hr. WOB 2 - 14 tonne. 2400 l/min/ 183 - 189 bar. 160 rpm / 12 - 24 kNm. ECD 1,40 SG. Took SCRs at 3303 m Maintained LCM background concentration" "On 2013-08-24, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3426m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3317 m to 3426 m, average ROP: 22 m/hr. WOB 5 - 12 tonne. 2400 l/min/ 188 - 195 bar. 160 rpm / 14 - 25 kNm. ECD 1,42 SG. Maintained LCM background concentration" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3546m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled 8 1/2' hole from 3426 m to 3546 m, average ROP: 22 m/hr. WOB 7 - 14 tonne. 2450 l/min/ 190 - 195 bar. 160 rpm / 18 - 22 kNm. ECD 1,42 SG. Maintained LCM background concentration Controlled ROP to 25 m/hr" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3546m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3576m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 8 1/2' hole from 3546 m to 3576 m, average ROP: 15 m/hr. WOB 7 - 14 tonne. 2450 l/min/ 190 - 195 bar. 160 rpm / 18 - 22 kNm. ECD 1,42 SG. Maintained LCM background concentration Controlled ROP to 25 m/hr" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3576m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Circulated and reciprocated string while Baker logging unit re-booted computer system" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3682m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: Drilled 8 1/2' hole from 3576 m to TD at 3682 m, average ROP: 15,7 m/hr. WOB 2 - 14 tonne. 2450 l/min/ 195 - 199 bar. 160 rpm / 11 - 26 kNm. ECD 1,42 SG. TD: 3682 m MD. Controlled ROP from 3626 - 3640 m: 15 m/hr / 3640 - 3682 m: 10 m/hr Maintained LCM background concentration" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3682m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Took final survey and downlinked" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3682m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated hole clean w/ 2450 l/min/ 197 - 194 bar, 140 RPM / 12 - 20 kNm, ECD 1,41 SG. Circulated first B/U Reciprocated string from 3682 - 3662 m" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3682m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Racked back one stand" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3682m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.2 hours. Operational details: Circulated hole clean w/ 2450 l/min/ 192 bar, 140 RPM / 21 - 20 kNm, ECD 1,40 SG, total 3 x B/U Reciprocated string from 3662 - 3327 m. Hold TBT for taking pressure points and re-logging" "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3505m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH 5 1/2' stands from 3665 m to 3505 m. Limited pulling speed to 2-3 min/stand. Made up TDS." "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3491m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: Re-logged section from 3503,3 to 3491 m w/ 2000 lpm, 135 bar, 60 rpm, 12 - 17 kNm." "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3544m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: RIH from 3491 m to 3544 m." "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3544m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.8 hours. Operational details: Made up TDS and re-logged section from 3544 to 3506 m w/ 2000 lpm, 135 bar, 60 rpm, 12 - 17 kNm." "On 2013-08-25, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3521m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.2 hours. Operational details: RIH to 3534 m. Took weights: 188 t up, 144 t down, 157 t rot. Performed 10 min. sticky test" "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3521m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Established circ. with 2000 lpm. 145 bar and positioned string at bit depth 3521,1 m. Adjusted string to neutral weight and hold stationary while taking TesTrak pressure point #1 at 3493 m - bad test." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3523m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH to 3523 m bit depth and positioned string. Performed second attempt for pressure point #1 - good test." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3511m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH to 3511 bit depth and positioned string. Took TesTrak pressure point #2 at 3480 m - bad test." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3512m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: RIH to 3512 m bit depth, positioned string. Performed second attempt for pressure point #2 - bad test." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3493m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH to 3493 m bit depth, positioned string. Took TesTrak pressure point #3 at 3462 m - good test." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3488m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH to 3488 m bit depth, positioned string. Took TesTrak pressure point #4 at 3457 m - good test." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3468m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH to 3468 m bit depth, positioned string. Took TesTrak pressure point #5 at 3437 m - good test." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3681m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH from 3468 m to 3681 m." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3681m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Circulated at TD to confirm free circulation before droping gyro." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3681m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Flowchecked well for 10 min, broke connection and loaded gyro tool." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3681m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Pump down gyro tool w/ 500 lpm, 26 bar, 20 rpm, 15 - 17 kNm." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3681m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 3 m3 slug and chased same." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3667m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH from 3681 m to 3667 m, slug did not work." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3667m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 5 m3 slug and chased same." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH w/ 8 1/2' BHA on 5 1/2' DP from 3667 m to 3225 m . Avg. tripping speed 354 m/hr. Restricted tripping speed and stoped when required for gyro station." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2982m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH, observed swabing at 3225 - 3220 m. Ran back in, volumes correct. Continued to POOH from 3225 m to 2982 m. Observed swabbing and overpull, trip tank increased. Wiped single, trip trank decreased to correct volume." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2940m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped OOH from 2982 m to 2940 m, 2200 lpm, 150 bar. Observed pressure increase while pulling. Reduced rate to 1350 lpm." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2982m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH from 2940 m - 2982 m for gyro overlap." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2580m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH from 2982 m to 2580 m inside the casing shoe. Avg. tripping speed 161 m/hr. Pulled wet, observed backflow, two slugs in annulus and float not holding. M/U TDS on every connection. Restricted speed due to gyro." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2580m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min, well static." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2499m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH from 2580 m to 2499 m, pulled wet. Observed backflow. Restricted speed due to gyro." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2499m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped slug and allowed levels to stabilise." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1650m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH from 2499 m to 1650 m. Avg. tripping speed 566 m/hr. Restricted speed due to gyro." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1770m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH from 1650 m to 1770 m. Re-surveyed as per Scientific intructions." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 480m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH from 1770 m to 480 m. Avg. tripping speed 1032 m/hr." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 480m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took rotational checks as per Scientific instructions." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 238m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH from 480 m to 238 m." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 238m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 10 min, well static. Removed PS21 slips." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 238m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: TBT with involved personnel for handling BHA." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 171m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH from 238 m to 171 m." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 171m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Broke double and layed out Scientific gyro toolstring." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pulled out to 50 m, layed out jar and accelerator." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Made announcement for handling RA sources, placed barriers. Baker RPS removed sources." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Plugged into tools and downloaded data. Dumped SoundTrak and TesTrak, OnTrak and CoPilot." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Cleaned and L/O BHA as per DD instructions." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Moved power rollers for 3 1/2' DP. Serviced TDS, dollies and both PRS." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed handling gear in slips and elevators from 5 1/2' to 3 1/2'." "On 2013-08-26, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Picked up, made up and RIH with open ended 3 1/2' cement stinger to 40 m." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 317m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Picked up, made up and RIH with open ended 3 1/2' cement stinger from 40 to 317 m." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 317m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Installed x/o, changed elevator inserts to 5 1/2', M/U stand and changed slip inserts to 5 1/2'." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1366m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: RIH w/ 3 1/2' cement stinger on 5 1/2' DP from 317 m to 1366 m." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1366m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Hydraulic fitting broke on auto slips. Replaced same." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2580m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 1366 m to 2580 m . Avg. tripping speed 1214 m/hr." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3141m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Took up and down weights. RIH in open hole from 2595 m to 3141 m. Restricted speed due to open endend DP in open hole." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3141m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke circ. with 1000 lpm, 20 bar." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3670m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: RIH from 3141 m to 3670 m . Avg. tripping speed 529 m/hr. Restricted speed due to open ended pipe." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3682m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: M/U TDS and washed in from 3670 m to bottom at 3682 m, 500 lpm, 27 bar. Tagged bottom." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3673m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Pulled back to 3673 m and circulated prior to cement job 2450 l/min/ 205 bar, 60 rpm. Reciprocated string." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3677m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Spaced out string, M/U cement assy and surface line. Tested line to 20/200 bar for 5 min." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3677m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Balanced cement plug #1 (3682 - 3387 m): Pumped 11,6 m3 of 1,60 SG spacer, 800 l/min/ 30 bar. Mixed and pumped 14 m3 of 1,90 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water. Zeroed volume counters. Pumped 3,6 m3 of 1,60 SG spacer. Displaced the cement with 29,1 m3 (1340 strokes) of mud, 2450 l/min/ 150 - 190 bar at 60 RPM." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3677m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke out surface line and L/D cement assy." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3387m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Pulled out of cement to 3387 m MD. Pulled dry, 2 - 3 min/ stand." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3387m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Circulated out excess cement and spacer 2450 l/min/ 203 bar, 80 rpm. Reciprocated string." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3387m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: M/U cement assy and installed surface line. Tested surface line to 20/200 bar for 5 min." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3387m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Balanced cement plug #2 (3387 m - 3092 m): Pumped 11,6 m3 of 1,60 SG spacer, 800 l/min/ 22 bar. Mixed and pumped 14 m3 of 1,90 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water. Zeroed volume counters. Pumped 3,61 m3 of 1,60 SG spacer from surface lines. Displaced the cement with 25,9 m3 (1193 strokes) of mud, 2450 l/min/ 170 bar at 60 RPM." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3387m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke off surface line and L/D cement assy." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pulled out of cement to 3090 m MD. Pulled dry, 2 -3 min/stand." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: Circulated out excess cement and spacer 2450 l/min/ 190 bar, 80 rpm. Reciprocated string." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: M/U cement assy and installed surface line. Tested surface line to 20/200 bar for 5 min." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Balanced cement plug #3 (3092 m - 2797 m): Pumped 11,6 m3 of 1,60 SG spacer, 800 l/min/ 10 - 22 bar. Mixed and pumped 14 m3 of 1,90 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water. Zeroed volume counters. Pumped 3,6 m3 of 1,60 SG spacer from surface lines. Displaced the cement with 22,6 m3 (1041 strokes) of mud, 2500 l/min/ 116 - 153 bar at 20 RPM." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke off surface line and L/D cement assy." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2795m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pulled out of cement to 2795 m MD. Pulled dry, 2 - 3 min/stand." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2795m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Circulated out excess cement and spacer 2500 l/min/ 180 bar, 60 rpm. Reciprocated string." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2795m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: M/U cement assy and installed surface line. Tested surface line to 20/200 bar for 5 min." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2795m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Balanced cement K/O plug #4 (2797 m - 2547 m): Pumped 11,6 m3 of 1,60 SG spacer, 800 l/min/ 20 bar. Mixed and pumped 13,3 m3 of 2,0 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water. Zeroed volume counters. Pumped 3,6 m3 of 1,60 SG spacer fro msurface lines. Displaced the cement with 22,2 m3 (1022 strokes) of mud, 2500 l/min/ 68 - 155 bar at 20 RPM." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2795m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke off surface line and L/D cement assy." "On 2013-08-27, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2545m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pulled out of cement. Pulled dry, 2 - 3 min/stand." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2545m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pulled out of cement to 2545 m MD. Pulled dry, 2 - 3 min/stand." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2545m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Circulated out excess cement and spacer 2500 l/min/ 172 bar, 60 rpm." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2430m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: POOH 2 stand, installed 2 sponge balls." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2430m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Circulated B/U and flushed string, 3300 l/min/ 255 bar at 120 rpm." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 317m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: POOH w/ 3 1/2' cement stinger on 5 1/2' DP." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 317m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed to 3 1/2' handling equipment." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: L/D 33 joints of 3 1/2 cement stinger." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed to 5 1/2' handling equipment, cleanend rigfloor." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1220m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: RIH to 1220 m with cement contaminated 5 1/2' stands." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1220m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Installed two sponge balls and flushed string, circ. 1,5 x string volume." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: POOH 5 1/2' stands and R/B same." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Removed PS21 slips, installed master bushing. Cleaned and cleared rigfloor. Function tested shear ram." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to run BOP test tool." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: M/U jet sub and BOP test tool. RIH w/ test tool. Jetted BOP/wellhead area at 138 m with 1500 lpm, 15 bar. Landed BOP test tool in wellhead. Meanwhile lined up and tested line to 20/345 bar 5/5 min." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Displaced BOP to water using cement unit." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.5 hours. Operational details: Tested BOP pipe rams and annular to 20 bar/ 5 min and 345 bar/ 10 min. Tested kill and choke lines to 20 bars / 5 min and 345 bar/ 10 min with water." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Opened BOP and displaced same with OBM." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: POOH and L/D BOP test tool. R/D handling equipment and cleared rig floor." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to M/U BHA." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: P/U and M/U 12 1/4' BHA in moduls as per Baker DD instructions" "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Plugged into tools and verfied same." "On 2013-08-28, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: P/U and M/U 12 1/4'' BHA including HWDP as per Baker DD instructions. Changed out one HWDP, damaged box observed." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: P/U and M/U 12 1/4' BHA, picked up HWDP, M/U jar and accelerator. Installed totco ring on top of accelerator." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Removed master bushing, installed PS21 slips." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1020m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH w/ 12 1/4' BHA on 5 1/2' DP from 247 m to 1020 m . Avg. tripping speed 618 m/hr." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1020m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Filled string and emptied TT" "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1860m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 1020 m to 1860 m . Avg. tripping speed 840 m/hr." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 1860m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Filled string and emptied TT." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2467m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH on 5 1/2' DP from 1860 m to 2467 m. Avg. tripping speed 810 m/hr." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2467m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Filled string and emptied TT." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2467m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Closed BOP and performed choke drill with both shifts, driller, AD and lead driller." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2507m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH from 2467 m to 2507 m, M/U TDS." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2555m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Washed from 2507 m to 2555 m w/ 2300 l/min, 120 bar, 20 RPM, 8 kNm. Tagged TOC at 2555 m." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled excess cement from 2555 m to 2595 m, WOB 6 tonne. 2300 l/min/ 123 bar. 20 rpm / 12 - 18 kNm. Reduced MW while drilling cement from 1,32 SG to 1,28 SG." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Downlinked set tools ribs off." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2604m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled from 2595 m to 2604 m in steps to clean shoe area and rathole with 2300 lpm, 113 bar, 20 rpm, 10 - 16 kNm, WOB 1-3 tonne. Softer cement in the rat hole." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2604m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Pulled back to 2588 m, tared CoPilot, downlinked to set tools for K/O, reamed in to 2604 m." "On 2013-08-29, at Well NO 15/9-F-1 A, a drilling event occurred at a depth of 2617m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Kicked off from 2604 m. Drilled from 2604 m to 2617 m, WOB 3 - 5 tonne. 2800 l/min/ 153 bar. 40 rpm / 13 - 17 kNm. Controlled ROP to 5 m/hr. Drilled as per Baker DD instructions. Bending moment and NB Inc. indicating successful sidetrack at 2617 m. Last Report on F-1 A, continue reporting on F-1 B." "On 2014-02-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled 17 1/2' hole from 1364 m to 1482 m with 4000 lpm, 230 bar, 130 rpm, 10-18 kNm, 6-8 WOB. ECD 1,44 SG, ROP 15-40 m/hr. Max gas 1,47 %. Obtained surveys as required" "On 2014-02-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated btm's up prior to perform check trip to inside 20' shoe with 4000 lpm, 230 bar, 130 rpm, 3-6 kNm. ECD 1,44 SG. Max gas 1,46 %. Reciprocated pipe." "On 2014-02-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. Well static." "On 2014-02-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1338m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 1482 m to 1338 m, 10 m inside 20' shoe. No drag observed when entered 20' shoe at 1348 m." "On 2014-02-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1442m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 1338 m to 1442 m. No drag observed when entered open hole at 1348 m." "On 2014-02-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Established circulation with 3500 lpm, 180 bar. Washed down from 1442 m to 1482 m. No drag or fill observed. Sent down link to autotrak." "On 2014-02-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1502m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 17 1/2' hole from 1482 m to 1502 m with 4000 lpm, 240 bar, 130 rpm, 5-8 kNm, 2-3 WOB. Controled ROP 12 m/hr. ECD 1,44 SG. Max gas 0,02 %. Obtained surveys as required." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1522m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 17 1/2' hole from 1502 m to 1522 m with 4000 lpm, 240 bar, 130 rpm, 7-11 kNm, 2-3 WOB. Controled ROP 12 m/hr due to waiting on weather to discharge cuttings to cuttings vessel. ECD 1,43 SG. Max gas 0,03 %. Obtained surveys as required." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1522m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Back reamed 1 single from 1522 m 1509 m. Took survey. Evaluated to drill ahead due to space for slurry in isotanks." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1522m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 1522 m, MW 1,4 SG, 30/40/50 stroks MP # 1 4/9/15 bar, MP # 2 5/8/16 bar." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1531m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 17 1/2' hole from 1522 m to 1531 m with 4000 lpm, 240 bar, 130 rpm, 5-7 kNm, 10 WOB. Controled ROP 12 m/hr due to waiting on weather to discharge cuttings to cuttings vessel. ECD 1,43 SG. Max gas 0,03 %. Obtained surveys as required." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1531m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Flow checked well due to 200 ltr gain observed in active pit. Well static." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1540m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 17 1/2' hole from 1531 m to 1540 m with 4000 lpm, 240 bar, 130 rpm, 6-15 kNm, 10 WOB. Controled ROP 12 m/hr due to waiting on weather to discharge cuttings to cuttings vessel.. ECD 1,44 SG. Max gas 0,02 %. Obtained surveys as required." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1540m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited one weather, not able to discharge cuttings to vessel due to bad weather. Circulated btm's up due to full iso tanks with 4000 lpm, 235 bar, 130-140 rpm, 3-6 kNm. ECD 1,43 SG. Max gas 0,02 %. Reciprocated pipe." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1509m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.8 hours. Operational details: WOW. R/B drilling stand # 33. Circulated well clean prior to pull inside 20' shoe with 4000 lpm, 227 bar, 130 rpm, 3-6 kNm. ECD 1,42 SG. Max gas 0,01 %. Reciprocated pipe from 1523 m to 1482 m." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1509m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. Flow checked. Well static." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1321m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW. POOH with 17 1/2' BHA on 5 1/2' DP from 1509 m to 1321 m, 27 m inside 20' shoe. No drag observed when entered 20' shoe at 1348 m. Performed kick drill with crew" "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1321m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.5 hours. Operational details: WOW. Performed service on traveling block, TDS and dolly. Serviced draworks brake. Cleaned and cleared rig floor. General service on drilling equipment and PM." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1321m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. Performed pre-job meeting with crew prior to RIH." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1525m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: WOW. RIH with 17 1/2' BHA on 5 1/2' DP from 1321 m to 1525 m. No drag observed when entered open hole at 1348 m." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1538m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Established circulation with 3700 lpm, 205 bar. Washed down from 1525 m to 1538 m. No drag or fill observed. Sent down link to autotrak." "On 2014-02-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1660m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 17 1/2' hole from 1540 m to 1660 m with 4200 lpm, 257 bar, 130 rpm, 6-8 kNm, 2-3 WOB. ROP 40 m/hr ECD 1,44 SG. Max gas 0,02 %. Obtained surveys as required. Observed change in formation at 1572/1629/1659 m. Blue Gardian left at 21:30 hrs unable to stay alongside on DP." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1684m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 17 1/2' hole from 1660 m to 1684 m with 4200 lpm, 257 bar, 130 rpm, 6-8 kNm, 2-3 WOB. ROP 40 m/hr ECD 1,44 SG. Max gas 0,02 %. Obtained surveys as required. Took survey at 1684 m as DD instruction. At 00:45 stopped drilling @ 1684 m, not able to discharge cuttings to vessel due to bad weather." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1684m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.8 hours. Operational details: Waited one weather, not able to discharge cuttings to vessel due to bad weather. Circulated btm's up due to full iso tanks with 4200 lpm, 257 bar, 130 rpm, 4-6 kNm. ECD 1,42 SG. Max gas 0,01 %. Reciprocated pipe from 1684 m to 1644 m. Total volume pumped 821 m3." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1684m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. Flow checked. Well static." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1496m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW. POOH with 17 1/2' BHA on 5 1/2' DP from 1684 m to 1496 m." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW. POOH with 17 1/2' BHA on 5 1/2' DP from 1496 m to 1320 m, 28 m inside 20' shoe. No drag observed when entered 20' shoe at 1348 m." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. M/U TDS to drill string and sent down link battery off." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. Performed pre-job meeting prior to manual handling. Remove PS-21 from rotary and install bushing and manual slips." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW. Removed PS-21 from rotary and installed bushing and manual slips." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. Performed kick drill with crew." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. Performed pre-job meeting prior to continue to M/U 13 3/8' casing and rack same in derrick." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.5 hours. Operational details: WOW. M/U 13 3/8' casing and R/B 4 stands in derrick. M/U shoe track, backer locked and tested floats with water." "On 2014-02-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.0 hours. Operational details: WOW. Change out Baker down link skid. Adjusted link tilt assy on TDS. Serviced upper and lower IBOPs on TDS. Performed service on BX-elevator and Iron roughneck. Pressure tested Baker down link skid to 190 bar. General rig service on drilling equipment. Cleaned drilling modul." "On 2014-02-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited one weather, not able to discharge cuttings to vessel due to bad weather. Performed high wind checks. General rig service and preventive maintenance on drilling equipment. Cleaned drilling modul, pump room, pit rom and shakers areas." "On 2014-02-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 13.0 hours. Operational details: WOW. General rig service and preventive maintenance on drilling equipment. Performed PM on rotary table. Performed service on PDM and HTS. Function tested 500 ton spider elevators. Performed service forw and aft PRS. Changed out electrical switch on BOP HPU pump # 1." "On 2014-02-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.2 hours. Operational details: WOW. Blue Guardian alongside on port side. Connected up hose to boat. Swaco started to back load cuttings from iso tanks. Disconnected hose from Blue Guardian. Removed manuelt slips and bushing from rotary. Installed PS-21 auto slips. Performed pre-job meeting with crew prior to RIH with BHA on 5 1/2' DP. Transferred 2 iso tank, 40 ton." "On 2014-02-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW. Established circulation in steps due to cold mud in to with 3500 lpm, 190 bar, 5-10 rpm. Sent down link to activate MWD battery on. Blue Guardian alongside on stb side. Connected up hose to boat. Swaco continued to back load cuttings from iso tanks." "On 2014-02-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1585m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: WOW. RIH with 17 1/2' BHA on 5 1/2' DP from 1320 m to 1585 m. No drag observed when entered open hole at 1348 m. Total amount of cuttings transferred to Blue Guardian 50 ton." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1645m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. RIH with 17 1/2' BHA on 5 1/2' DP from 1585 m to 1645 m." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1684m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW. Established circulation in steps to with 3650 lpm, 220 bar. Sent down link to activate ribs. Washed down from 1645 m to 1684 m, tagged TD with 1 ton. No fill or draque observed." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1684m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Established drilling parameters with 4000 lpm, 255 bar, 130 rpm, 6-8 kNm. Took up down weight, 140/123 ton. Free rotating weight 130 ton." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1692m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 17 1/2' hole from 1684 m to 1692 m with 4000 lpm, 273 bar, 130 rpm, 9-12 kNm, 7 WOB. ROP 30 m/hr ECD 1,44 SG. Max gas 0,02 %. Obtained surveys as required. Observed 500 ltr gain in active pit." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1692m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Flow checked well. Well static." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1723m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 17 1/2' hole from 1692 m to 1723 m with 4200 lpm, 270 bar, 130 rpm, 6-28 kNm, 6 WOB. ROP 30 m/hr ECD 1,44 SG. Max gas 0,01 %. Obtained surveys as required." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1723m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 1723 m, MW 1,4 SG, 30/40/50 stroks MP # 1, 7/12/19 bar, MP # 2, 7/12/20 bar." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1776m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled 17 1/2' hole from 1723 m to 1776 m with 4200 lpm, 270 bar, 130 rpm, 10-18 kNm, 8-12 WOB. ROP 35 m/hr ECD 1,44 SG. Max gas 0,03 %. Obtained surveys as required." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1864m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 17 1/2' hole from 1776 m to 1864 m with 4200 lpm, 270 bar, 130 rpm, 10-18 kNm, 8-12 WOB. ROP 35 m/hr ECD 1,44 SG. Max gas 0,03 %. Obtained surveys as required." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1864m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited one weather, not able to discharge cuttings to vessel due to bad weather. Circulated btm's up due to full iso tanks with 4300 lpm, 285 bar, 130 rpm, 4-10 kNm. ECD 1,43 SG. Max gas 0,06 %. Reciprocated pipe from 1684 m to 1644 m. Total volume pumped 282 m3." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1713m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW. Pumped out of hole from 1864 m to 1713 m with 4000 lpm, 240 bar." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1713m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Flow checked well. well static." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1319m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: WOW. POOH with 17 1/2' BHA on 5 1/2' DP from 1713 m to 1319 m, 29 m inside 20' shoe. No drag observed when entered 20' shoe at 1348 m." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1319m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Serviced upper IBOP." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1864m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: WOW. RIH with 17 1/2' BHA on 5 1/2' DP from 1319 m to 1848 m. No drag observed when entered open hole at 1348 m. Filled pipe. Established circulation and washed down 1864 m." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1924m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 17 1/2' hole from 1864 m to 1924 m with 4350 lpm, 284 bar, 130 rpm, 9-12 kNm, 7-10 WOB. ROP 40 m/hr ECD 1,43 SG. Max gas 0,02 %. Obtained surveys as required." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1924m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 1924 m, MW 1,4 SG, 30/40/50 stroks MP # 1. 8/14/21 bar, MP # 2. 8/13/21 bar." "On 2014-02-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2080m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled 17 1/2' hole from 1924 m to 2080 m with 4350 lpm, 284 bar, 130 rpm, 9-12 kNm, 7-10 WOB. ROP 40 m/hr ECD 1,44 SG. Max gas 0,02 %. Obtained surveys as required. Stringers @ 1991 m, 1998 m, 2024 m, 2033 m, 2046 m, 2051 m." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2088m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 17 1/2' hole from 2080 m to 2088 m with 4300 lpm, 288 bar, 130 rpm, 8-18 kNm, 12 WOB. ROP 40 m/hr ECD 1,44 SG. Max gas 0,01 %. Obtained surveys as required." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2088m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.2 hours. Operational details: Waited one weather from 00:45 to 04:15 hrs. Not able to discharge cuttings to vessel due to bad weather. Circulated well clean with with 4200 lpm, 265 bar, 130 rpm, 4-6 kNm. ECD 1,44 SG. Max gas 0,02 %." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2120m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 17 1/2' hole from 2088 m to 2120 m with 4300 lpm, 280 bar, 130 rpm, 8-18 kNm, 12 WOB. ROP 30 m/hr ECD 1,44 SG. Max gas 0,01 %. Obtained surveys as required." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2209m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled 17 1/2' hole from 2120 m to 2209 m with 4300 lpm, 280 bar, 130 rpm, 8-18 kNm, 12 WOB. ROP 40 m/hr ECD 1,44 SG. Max gas 0,01 %. Obtained surveys as required." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2209m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 2209 m, MW 1,4 SG, 30/40/50 stroks MP # 1, 8/15/21 bar, MP # 3, 8/14/22 bar." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2209m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed drops check and serviced elevator, Meanwhile took survey." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2514m. The activity was categorized as 'drilling -- drill' and lasted for 13.0 hours. Operational details: Drilled 17 1/2' hole from 2209 m to 2514 m with 4200 lpm, 275 bar, 140 rpm, 10-28 kNm, 12-20 WOB. ROP 40 m/hr ECD 1,43 SG. Max gas 0,4 %. Obtained surveys as required. Took survey on bottom." "On 2014-02-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2514m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Started to circulate hole clean with 4200 lpm, 273 bar, 140 rpm, 8-12 kNm. ECD 1,43 SG. Max gas 0,08 %." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2451m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: Circulate hole clean with 4200 lpm, 270 bar, 140 rpm, 8-12 kNm. ECD 1,41 SG. Max gas 0,05 %. Circulated hole clean and swept hole with 2 x 5 m3 hi-vis. R/B 1 stand for each stand btm's up to 2451m. Total volume pumped 900 m3." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated and conditioned mud weight to 1,41 SG. R/B 1 stand for each stand btm's up to 2410 m. Total volume pumped 450 m3." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2451m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Sent down link to rips off. R/B stand to 2410 m." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2451m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well. Well static. Meanwhile performed pre-job meeting with crew prior to POOH. Cheched dies in PRS." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2209m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 2451 m to 2209 m. 158 ton up weight no drag observed." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2209m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 4 m3 of 1,8 SG slug." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2088m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 2209 m to 2088 m. First 5 stand pulled wet." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2088m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Problem with aft PRS, reset and parked same. Use fwd PRS, unplanned release of stand into derrick. Hold SJA meeting and Tool box talk prior to retrieving stand. Retrieved stand from Derrick as per plan/Procedure. Rotated drill string every 15/30 mins ,4 kNm free torque observed." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 2088 m to 1320 m, 28 m inside 20' shoe. No drag observed when entered 20' shoe at 1348 m." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1320m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well. Well static." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1220m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Serviced drill floor equipment." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 270m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 1320 m to 270 m. 600 m/hr." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 270m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well prior to pull BHA through BOP. Well static." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 160m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 17 1/2' BHA from 270 m to 160 m. Dropped 2 7/8' drift into HWDP." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 160m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed PS-21 from rotary. Installed master bushing and manuel slips." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 17 1/2' BHA from 160 m to 109 m. Performed pre-job meeting with crew prior to start handling BHA." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to start handling BHA." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 17 1/2' BHA from 109 m to 23 m." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Plugged into MWD tool and downloaded data." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 17 1/2' BHA from 23 m and L/O MWD and autotrak on deck." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor of excess equipment." "On 2014-02-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to pull nominal seat protector." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: M/U jet assy to HWDP and rih to 44 m. Performed pre-job meeting prior to pull nominal seat protector." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 132m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U W.B RRT, M/U STD HWDP. Function tested as per GE instructs, RIH to 132 m." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 132m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: M/U TDS, Jet wash W.H from 133 m to 140 m 3 x passes with 2000l lpm, 25 bar." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: M/U TDS to string. RIH from 133 m to 138.9 m. Engaged W.B RRT as per G.E instructions. Set down 7 ton, P/U 3-5 ton overpull, W.B disengaged." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 112m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: POOH from 138 m to 112 m. M/U TDS to string. Jet washed 3 x passes ( Jet from 140m to 133 m ) with 2000 lpm, 27 bar." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 46m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: POOH from 112 m to 46 m." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 46m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior L/O W.B and W.B RRT." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 46m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Released W.B and reset RRT as per G.E instructions L/O same." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH from 46 m, R/B and L/O jet sub assy. Meanwhile hold pre-job meeting prior to perform service TDS." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed servic on TDS." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rig up 13 3/8' casing equipment." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: R/U 13 3/8' casing equipment. P/U casing tong and R/U same." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with new crew prior to rig up 13 3/8' casing equipment." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: R/U 13 3/8' casing equipment. Removed BX-elevator and rotating arm. Installed Archer circulating tool to TDS. Installed 500 ton elevator. Checked space out for circulating tool. Installed FMS slips and attached hoses, function tested same." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U shoe track and run 13 3/8' casing." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U 13 3/8' shoe track and M/U and thread locked to joint # C4 to 50 m." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1188m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 13 3/8' casing stand from 50 to 1188 m. Running speed 189,5 m/hr. Filled every stand while RIH. Recorded up/down weight prior to entering open hole." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1188m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to run 13 3/8' casing." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1188m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Checked casing equipment. Greased slips, elevator and casing tong." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 13 3/8' casing stand from 1188 to 1348 m. Running speed 128 m/hr. Filled every stand while RIH. Recorded up/down weight prior to entering open hole, 185/170 ton." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1848m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 13 3/8' casing stand from 1348 to 1848 m. Running speed 166,5 m/hr. Filled every stand while RIH. No drag observed when entered open hole at 1348 m." "On 2014-02-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1848m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Greased elevator and checked casing tong." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with 13 3/8' casing stand from 1848 to 2362 m. Running speed 166,5 m/hr. Filled every stand while RIH. Counted remaining joints on deck." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to R/D 500 ton elevator and B/O fill up tool from TDS. Install BX-elevator." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: R/D 13 3/8' casing equipment. R/D 500 ton elevator and B/O fill up tool from TDS. Installed BX-elevator." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U and M/U 13 3/8' casing hanger. Removed seal protection and inspected Hanger seal area." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2372m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: R/D 13 3/8' casing equipment. Removed FMS slips from rotary. Lowered 13 3/8' casing hanger below rotary to 2372 m. Installed master bushing. Installed inner bushings and manual slips. R/D casing tong." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2413m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 13 3/8' casing on 5 1/2' HWDP landing string to 2413 m." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2453m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 13 3/8' casing on 5 1/2' HWDP landing string from 2413 m to 2453 m." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Washed down 13 3/8' casing on 5 1/2' HWDP landing string with 500 lpm,13 bar from 2453 m to 2505 m. Took weight @ 2493 m 6-12 ton." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: B/U double from stand and R/B in fwd PRS." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: P/U and M/U cement head. Installed valves and cement line." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: M/U TDS and established circulation with 500 lpm, 18 bar. Landed off casing at 2507,8 m and sat down all weight. Set hanger according to Vetco procedure. Took 2-3 ton tension." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: Circulated 1 x casing 195 m3 with 2500 lpm, 35 bar. No losses observed. Performed pre-job meeting prior to perform cement job. Surface line tested to 27 bar. Trapped 20 bar behind lower IBOP." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pumped 25 m3 of 1,6 SG spacer with 2100 lpm, 23 bar through TDS with rig pumps. Trapped 20 bar behind lower IBOP. Released dart for bottom wiper blug." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Mixed and pumped 30,9 m3 of 1,92 SG cement slurry with 636 lpm, 18 bar. Released top dart. Displaced the cement to the rig floor with 1,5 m3 of drill water. Zeroed stroke counters. Observed bottom dart landed in bottom wiper plug after 970 ltr. Shear pressure 117 bar. Observed top plug shared after 700 ltr, 64 bar. Full returns during cementing." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Released top dart and displaced cement using rig pumps with 2500 lpm, 8 bar. Decreased to 2000 lpm prior to shear ,Sheared btm plug at 135 bar, 6686 stroke. Top plug landed at 8250 stroke. FCP 10 bar. Full returns during displacement." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pressure tested 13 3/8' casing to 270 bar for 10 min using rig pumps. Test ok. Bleed off pressure to trip tank to 22 bar observed for pressure build up, non observed. Bled off remaining pressure to zero. Observed for back flow, no flow observed." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Flushed lines from cement unit to Rig floor until clean. Removed surface lines and control lines from cement head." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Set seal assembly as per Vetco instruction. Flushed lines, performed line test 345 bar, 70 ltr pumped and received. Closed annular and Install seall assy as per Vetco procedure. applied 20/207 bar to stroke down MS seal. Volume pumped 317 ltr, volume recieved 306 ltr. Tested seal assy as per Vetco Procedure with 45 ton overpull. Close Annular and pressure test MS seal assy to 20/345bar 5/10 min as per procedure. Observed 2 bar drop off on low pressure test, bled off pressure and functioned annular open/close and performed re test. Observed drop on low pressure test with annular, bled off pressure. Closed Lower pipe pams and attempt to test seal assy no success." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Evaluated leak on line test. Test surface lines 20/345bar 5/10min, function all valves. Lined up on cement line also test line to eliminate posible leaking valves. Good test." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Closed annular and pressure tested seal assy 20/345 bar, 5/10 min." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released PADPRT as per Vetco procedures POOH from 139 m to 137 m." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to B/O and L/D cement head and PADRPT." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: B/O and L/D cement head and PADRPT." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor of excess equipment." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Installed 2 sponge balls in string circulated pipe clean weth 3500 lpm, 42 bar." "On 2014-03-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with PADRPT from 137 m and L/D same." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to pressure test BOP." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Performed line test to 270 bar, 5 min. Closed BSR, pressure tested same to 20/270 bar, 5/10 min." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U jet sub assy to stand HWDP RIH to 44 m. M/U WBRRT to W.B, M/U to stand HWDP. Function test WBRRT engage / disengage." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: RIH with wear bushing and installed same138,9 m. POOH and L/D W.B running tool." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.2 hours. Operational details: Pressure tested BOP rams, HCR, kill and choke lines to 20/345 bar, 5/10 min. according to procedure. Function tested BOP from drillers console. Meanwhile changed out Ibop and saver sub inbetween tests." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Pressure tested BOP rams, HCR, kill and choke lines to 20/345 bar, 5/10 min. according to procedure. Meanwhile changed out Ibop and saver sub inbetween tests." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to perform BOP test and change out IBOP and saver sub on TDS." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: Pressure tested BOP rams, HCR, kill and choke lines to 20/345 bar, 5/10 min. according to procedure. Meanwhile changed out Ibop and saver sub inbetween tests. Released wear bushing running tool as per Vetco instruction and L/U pup joint" "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: Changed out IBOP and saver sub on TDS." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U swedge and test line to TDS." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: M/U swedge and test line to TDS. Tested connections and Ibop/saver sub to 20/345 bar, 5/10 min. R/D test assy from TDS." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: POOH with jet sub and WBRT from 42 m to surface. Resetted WBRT as per Vetco procedure. L/O WBRT and Jet sub." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Cleaned and cleared drill floor for excess equipment. B/O TIW from casing circulating swedge." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U 12 1/4' BHA." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 5m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: P/U and M/U 12 1/4' drilling assembly to 5 m." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 5m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with new crew prior to M/U 12 1/4' BHA." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: P/U and M/U 12 1/4' drilling assembly to 24 m." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pulled back to 15 m. Plugged into MWD and uploaded MWD." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: P/U and M/U 12 1/4' drilling assembly from 24 to 32 m." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed insterts in BX-elevator to 6 5/8'." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: P/U and M/U 12 1/4' drilling assembly from 32 m. P/U 6 5/8' HWDP, discovered that box on X-O from 6 5/8' reg x 5 1/2' FH box was not full bore." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: B/O X-O and L/O single 6 5/8 HWDP and X-O. Continued to M/U modified BHA according plan." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed insterts in BX-elevator to 51/2'." "On 2014-03-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 51m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: M/U 12 1/4' drilling assembly to 51 m." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 192m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: M/U 12 1/4' drilling assembly from 51 m to 192 m including HWDP." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 192m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed master bushing and installed PS-21 auto slips in rotary. Emptied trip tank." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 998m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH 12 1/4' drilling assembly on 5 1/2' DP from 192 m to 998 m. Filled pipe every 1000 m." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 998m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Connected TDS to drill string and filled pipe." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1968m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH 12 1/4' drilling assembly on 5 1/2' DP from 998 m to 1968 m." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1968m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Connected TDS to drill string and filled pipe." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH 12 1/4' drilling assembly on 5 1/2' DP from 1968 m to 2100m." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2372m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH 12 1/4' drilling assembly on 5 1/2' DP from 2100 m to 2372 m." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2372m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed choke drill with crew prior to drill out 13 3/8' shoe track." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2452m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH 12 1/4' drilling assembly on 5 1/2' DP from 2372 m to 2452 m." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2474m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: M/U TDS and established circulation with 1000 lpm, 20 bar and washed down. Tagged top of cement at 2473,8 m with 3 ton." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2474m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Established drilling parameters to 3000 lpm, 190 bar and down linked to autotrak." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2475m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled out plug and cement from 2473,8 m to 2475 m with 3000 lpm, 190 bar, 40 rpm, 7-10 kNm, WOB 2-4 ton. Simultaneously displaced well to 1,28 SG OBM. Cement cuttings to skips." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2474m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: WOW. Waited on deck crane. Pick up off bottom due to unable to arrange cutting skip with crane. Continued to displace well to 1.28 SG OBM with 3000 lpm, 190 bar. Cement cuttings to skips." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2474m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: WOW. Took SCR @ 2474 m, MW 1,28 SG, 30/40/50 stroks MP # 1, 11/16/24 bar, MP # 3, 11/16/25 bar." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2474m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW. Continued to circulate and condition mud weight to 1,28 SG. Cement cuttings to skips." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2507m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled out shoe track from 2475 m to 2507 m with 3000 lpm, 166 bar, 40 rpm, 6-10 kNm, WOB 4-6 ton. Max ECD 1,43 SG. Cement cuttings to skips." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2514m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled and cleaned rat hole in steps of 1-2 m from 2507 m to 2514 m with 3000 lpm, 166 bar, 40 rpm, 6-10 kNm, WOB 2-7 ton. Max ECD 1,34 SG. Cement cuttings to skips." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 3 m new formation from 2514 m to 2517 m with 3000 lpm, 166 bar, 40 rpm, 6-10 kNm, WOB 2-7 ton. Max ECD 1,34 SG. Cement and cuttings to skips." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Back reamed from 2517 m to 2506 m with 3000 lpm, 166 bar, 40 rpm, 6-10 kNm. No drag observed when entered shoe. Reamed back to bottom at 2517 m. Stopped pumping and rotating. Pulled back into 13 3/8' shoe several times no drag observed." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated well clean and contitione mud weight to 1,28 SG with 3500 lpm, 200 bar, 20 rpm, 6-8 kNm. Max ECD 1,34 SG. prior to perform FIT. Reciprocated drill string from 2506 m to 2493 m. Meanwhile lined up and tested lines from cement unit to 120 bar / 5 min." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2506m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.8 hours. Operational details: Closed well in on UPR and lined up to pump down string and Lower Kill line. Flushed system. Performed FIT to 66 bar using 1,28 sg mud, 1,55 sg EMW. Pumped 1045 liter from 4,8 bar to 66 bar at cement unit with 100 lpm. Bled back 807liter." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2506m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Circulated with 3000 lpm, 160 bar. Downlink to receive FIT data from MWD. Received 1,605 SG." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Washed down from 2491 m to 2517 m with 500 lpm, 67 bar. No drag observed when entering open hole." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Established drilling parameters to 3000 lpm, 160 bar, 80 rpm. Downlink to activate Ribs." "On 2014-03-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2646m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled 12 1/4' hole from 2517 m to 2646 m with 3850 lpm, 250 bar, 120 rpm, 12-16 kNm, 4-5 WOB. ROP 35 m/hr ECD 1,33 SG. Max gas 0,3 %. Obtained surveys as required. Bled in 4 m3 LCM in activ system for each stand drilled. Not able to discharge cuttings to cutting vessel due to bad weather. Take cuttings into iso tanks." "On 2014-03-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2674m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 12 1/4' hole from 2646 m to 2674 m with 3850 lpm, 250 bar, 120 rpm, 12-16 kNm, 6-12 WOB. ROP 30 m/hr ECD 1,32 SG. Max gas 0,2 %. Obtained surveys as required. Bled in 4 m3 LCM in activ system for each stand drilled. Take cuttings into iso tanks." "On 2014-03-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2755m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled 12 1/4' hole from 2674 m to 2755 m with 3850 lpm, 250 bar, 120 rpm, 15-20 kNm, 16 WOB. ROP 30 m/hr ECD 1,32 SG. Max gas 0,2 %. Obtained surveys as required. Added 4 sacks LCM in activ system for each stand drilled. Not able to discharge cuttings to cutting vessel due to bad weather. Take cuttings into iso tanks." "On 2014-03-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2775m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 12 1/4' hole from 2755 m to 2775 m with 3850 lpm, 253 bar, 120 rpm, 12-16 kNm, 5-13 WOB. ROP 20 m/hr ECD 1,31 SG. Max gas 0 %. Obtained surveys as required. Added 4 sacks LCM in activ system for each stand drilled" "On 2014-03-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2775m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 2775 m, MW 1,28 SG, 30/40/50 stroks MP # 2, 8/14/22 bar, MP # 3, 9/15/21 bar." "On 2014-03-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3056m. The activity was categorized as 'drilling -- drill' and lasted for 14.5 hours. Operational details: Drilled 12 1/4' hole from 2775 m to 3056 m with 3850 lpm, 260 bar, 120 rpm, 12-16 kNm, 12-14 WOB. ROP 20-30 m/hr ECD 1,31 SG. Max gas 0,15 %. Obtained surveys as required. Added 4 sacks LCM in activ system for each stand drilled. Take cuttings into iso tanks from 12:30 hrs. Section TD at 3056 m" "On 2014-03-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3056m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Worked torque out of string. Took survey and sent downlink." "On 2014-03-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3056m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated hole clean with 3880 lpm, 242 bar, 140 rpm, 11-16 kNm, ECD 1,31 SG. Max gas 0,1%. Circulated total 2 B/U, 409 m3. Take cuttings into iso tanks." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3056m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Circulated hole clean with 3880 lpm, 242 bar, 140 rpm, 11-16 kNm, ECD 1,31 SG. Max gas 0,1%. Circulated total 1 B/U, 207 m3. Downlink ribs off." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3056m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well. Well static. North Purpose alongside. Connected hose to boat. Swaco started to back load cuttings from Iso tanks. Started to take onboard casing." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3042m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pulled back to 3042 m. Set slips, B/O DP single and retracted TDS prior to drop gyro. Problem with Gyro communication prior to P/U. M/U DP single." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3042m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Circulated hole clean with 3880 lpm, 245 bar, 40 rpm, ECD 1,31 SG. Max gas 0,1%. Meanwhile troubleshoot on gyro. No success." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pulled back to 3017 m. B/O TDS and racked stand." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. Well static." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2923m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 12 1/4' BHA from 3017 m to 2923 m. Pulled 5 stands wet." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2923m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: M/U TDS pumped 4 m3 slug, chased same with 4.5 m3 1.28 SG mud." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2491m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 12 1/4' BHA from 2923 m to 2491 m inside 13 3/8' shoe. Tight spot at 2811 - 2795 m, 20 - 25 Mt overpull." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2491m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. Well static." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2126m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH w/ 12 1/4' BHA on 5 1/2' DP from 2491 m to 2126 m." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2126m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: M/U TDS and pumped 4 m3 1,61 sg slug and chased same with OBM." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 232m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH w/ 12 1/4' BHA on 5 1/2' DP from 2126 m to 232 m. Avg. tripping speed 758 m/hr." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 232m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Well static. Meanwhile held TBT for POOH and L/O 12 1/4' BHA." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' BHA. R/B HWDP stands." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed master bushings." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 12 1/4' BHA. R/B and L/O as per Baker DD instructions." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Plugged into OnTrak and CoPilot and downloaded memory data." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: L/D 12 1/4' BHA modules as per Baker DD instructions. Drained motor prior to L/O." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for retrieving wearbushing." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 132m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U jet sub and WBRRT. Function tested same and RIH to 132 m." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 142m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U TDS and jetted wellhead area from 138 m to 142 m. 1700 l/min, 12 bar. Made 3 passes." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH from 142 m to 186 m. Engaged WB at 138 m and released same as per GE Vetco instructions with 120 Mt on weight indicator." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: B/O TDS and installed 2 7/8' drift." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH from 186 m to 138 m. Jetted wearbushing setting area with 1700 l/min, 13 bar. Made 3 passes." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH to 50 m, removed bushings. Disengaged wearbushing and L/O same. Re-set WBRRT and L/O same. POOH to surface and L/O jet sub assy." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U HWDP stand, RIH, B/O and L/O single on deck." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for P/U and R/B casing hanger." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: P/U casing hanger. M/U to double HWDP and racked back in derrick." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed TBT for manriding. Meanwhile cleared and cleaned rig floor." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed manriding and serviced drilling equipment." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for R/U casing running equipment." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: R/U handling equipment for 9 5/8' casing. Installed pumping sub on TDS. Installed 9 5/8' elevator inserts. Moved Weatherford powertong into position and installed same. Prepared swedges/FOSV. Installed FMS." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for running 9 5/8' x 10 3/4' casing." "On 2014-03-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U 9 5/8' shoe joint from HTS. Checked float shoe for flow-through. M/U shoe joint and intermediate/landing collar double from derrick. Thread locked connection." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 75m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Filled shoe track. P/U 9 5/8' centralized stand #8 from derrick. M/U same to shoe track. RIH from 38 to 75 m." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 518m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 VamTop casing stands from 75 m to 518 m (8 stands with centralizers). Filled casing every stand. Average running rate 11 joints/hr." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 924m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 9 5/8' casing stands from 518 m to 924 m. Filled casing every stand. Average running rate 18 joints/hr." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 924m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Installed rollers on HTS. Checked and serviced Weatherford tong. Greased and checked elevators and PDM." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 936m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U joint from deck and RIH with 9 5/8' casing from 924 m to 936 m." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 936m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT with new crew for running 9 5/8' casing from deck." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2005m. The activity was categorized as 'drilling -- casing' and lasted for 11.8 hours. Operational details: RIH with 9 5/8' 53,2 ppf P110 VamTop casing from 936 m to 2005 m. Filled casing every 5th joint. Average running rate 7,6 joints/hr." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2005m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT with new crew for running 9 5/8' casing from deck." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2029m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 9 5/8' casing from 2005 m to 2029 m." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2029m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Changed rollers and turned PDM head to pick up casing from starboard forward bay on cantilever." "On 2014-03-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2337m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 VamTop casing from 2029 m to 2337 m. Filled casing every 5th joint. Average running rate 7,3 joints/hr." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 VamTop casing from 2337 m to 2410 m. Filled casing every 5th joint. Average running rate 8 joints/hr." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for changing handling equipment." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: R/D BX elevators. B/O pump-in swage from TDS. R/U 10 3/4' spider elevators and function tested same. Installed fill-up and circulation tool." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U 10 3/4' x 9 5/8' x-over joint from HTS using forwards PRS. Unable to lower spider elevator over x-over joint. Fill-up tool sealing element OD to large. L/D fill-up tool. Checked second tool, seal element not installed. Decided to continue w/o tool." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Attempted to M/U X-over joint, lower part of X-over joint body 11 3/4' OD. Spun in X-over using chain tongs. Lowered connection in rotary. Made several attempts to M/U connection with Weatherford power tong. Evaluated make-up graph and discussed situation with onshore organization. Accepted connection." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Removed Weatherford 9 5/8' FMS and installed 10 3/4' PS30 slips. Removed excess equipment from setback area. Changed from spider elevator to BX3 elevator as fill up tool did not fit into casing and spider elevator hanging up on box on 10 3/4' casing. Installed 10 3/4' inserts." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT with new crew for running 10 3/4' casing stands from derrick." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Function tested handling equipment." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: In preparation for high wind speeds, lifted cement head and HWDP single on HTS and re-arranged equipment on rig floor." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Troublshot leaking solenoid valve on TDS." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2496m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 10 3/4' 65,7 ppf P110 VamTop casing from 2410 m to 2496 m. Filled casing every stand." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2902m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 10 3/4' casing in from 2496 m to 2902 m. Entered open hole at 2507 m. Filled casing every stand. Average running rate 9,6 joints/hr. Hole in good condition. Took 11 MT weight on last 2 m." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2902m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed handling equipment to 5 1/2'. P/U and M/U casing hanger." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2940m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Removed PS30 slips, installed outer ring. Removed seal assembly protection. Installed master bushing and RIH to 2940 m. Rigged down casing tong." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2953m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U 5 1/2' HWDP single from HTS and RIH from 2940 m to 2953 m." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3034m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 9 5/8' x 10 3/4' casing on 5 1/2' HWDP landing string from 2953 m to 3034 m." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3045m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Took 20 MT weight. Picked up with 35 MT overpull. Established circulation w/ 200 l/min and increased flow to 500 l/min, 20 bar. Washed casing down from 3034 m to 3045 m. Set slips, B/O TDS, B/O double and racked same." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3045m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U cement head from HTS. M/U cement hoses. M/U cement stand to landing string." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Established circulation with 500 l/min. Landed casing hanger in wellhead as per GE Vetco instructions." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Increased flow in 250 l/min steps to 1600 l/min/ 37 bar. Held TBT for cement job. Tested rig up prior to cement job." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Decreased flow to 1500 l/min/ 35 bar due to potential slight losses. Circulated tot. 115 m3." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Transfered 20 m3 OBM between pits, bypassed sand traps. Displaced cement line with 1 m3 DW." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 20 m3 1,60 sg spacer w/ 1500 l/min, 38 bar." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Confirmed line-up. Dropped bottom dart. Mixed and pumped 15 m3 1,90 sg cement slurry with 630 l/min. Bottom plug released after 900 ltr/119 bar." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Dropped top dart and displaced same with 1,5 m2 DW from cement unit. Top wiper plug released after 920 ltr/106 bar." "On 2014-03-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Displaced cement with 1500 l/min and 14 - 47 bar 1,28 sg OBM using rig pumps. Encountered losses and reduced rate to 1400 l/min, 48 - 54 bar. Reduced rate further to 1300 l/min, 52 - 71 bar. Bottom plug sheared after 4490 strokes with 153 bar. Reduced rate on last 2 m3 to 500 l/min, 53 bar. Bumped top plug after 5170 strokes/112 m3 (94,9 % eff). Lost 8 m3 during displacement." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Increased pressure to 123 bar for 5 min after bumping top plug. Lined up to cement unit and equalized pressure." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressure tested casing to 345 bar for 10 mins. Pumped 1168 lts (130 bar to 345 bar), bled back 2161 lts (345 bar to 0 bar). Checked for back flow at cement unit. Floats holding." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: WOC to bullhead B-annulus to brine. Meanwhile R/D casing running equipment and performed maintenance on drilling equipment." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed TBT for bullheading B-annulus." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up manifold and confirmed line-up. Closed MPR." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 6.2 hours. Operational details: Started pumping 1,10 sg brine with 250 l/min. Fractured formation after 3550 ltr pumped with 63 bar. Staged rate up to 1000 l/min and bullheaded 95 m3 of 1,10 sg brine followed by 20 m3 of SW. FCP: 112 bar. Stopped pumping and monitored pressure response for 30 min. Final SIP: 72 bar. Bled pressure back in 25 bar steps to trip tank. Bled back 18 m3." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set 10 3/4' seal assembly as per GE Vetco instructions. Verified distance between pipe marks (8 1/4')." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed line test to 20/345 bar for 5/10 min. Meanwhile performed TBT for testing seal assembly." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Closed MPR. Pressured up to 207 bar and stroked down seal assembly. Pumped 280 lts, bled back 196 lts. Opened MPR. Picked up on string, verified pipe mark distance." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressure tested seal assembly to 20/345 bar for 5/10 min. Good test, pumped/bled back 325 lts." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released PADPRT as per GE Vetco instructions." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Flowchecked well, well stable." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Displaced riser to 1,28 sg OBM w/ 2000 l/min/ 13 bar. Emptied TT." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: B/O and L/D cement head. P/U HWDP double from setback and M/U same to landing string." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with PADPRT on 5 1/2' HWDP LS from 140 m to surface." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Inspected PADPRT, lead impression blocks with good indication. L/O RT." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Removed elevators and R/U chains and bridle to pull diverter." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to removing diverter." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Removed master bushings. Pulled diverter, landed and secured same on setback." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Removed nuts from slick joint. Lifted same to rig floor using dual-lift arrangement with PRS and tugger." "On 2014-03-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Commenced annular BOP repair. Removed annular top housing using dual lifting arrangement with chain hoists and moonpool overhead crane." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: Removed annular top housing. Emptied annular from mud. Replaced seal in annular. Meanwhile performed maintenance on drilling equipment." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Re-assembled annular. Meanwhile performed maintenance on drilling equipment." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Installed slick joint and diverter." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Performed TBT for testing BOP." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Lined up and tested surface lines to 20/345 bar for 5/10 min. Meanwhile: Performed maintenance on drilling equipment. Load tested port side crane to 55 MT." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.0 hours. Operational details: Tested BOP to 20/345 bar for 5/10 min against well. Function tested BOP. Tested kill and choke lines to 20/345 bar for 5/10 min. Meanwhile: Performed maintenance on drilling equipment. Load tested port side crane to 55 MT." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Performed TBT for installing wear bushing." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: M/U jet sub and wear bushing RT. RIH with same. Jetted BOP/wellhead area. Landed wear bushing in wellhead." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: B/O 5 1/2' DP double and R/B same. Installed pup joint. Installed pumping sub and 5k hose on TDS. Lined up for pressure testing." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: Tested BOP and surface equipment to 20 bar/ 5 min and 345 bar/ 10 min." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: R/D pump in sub and 5k hose." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: POOH with WB RT, re-set and L/O same. L/O jet sub assy." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor, inspected TDS for PDO and changed elevator inserts to 5'." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed TBT for M/U 8 1/2' RSS BHA." "On 2014-03-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: P/U and M/U 8 1/2' RSS BHA modules as per Baker DD instructions." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 39m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: P/U and M/U 8 1/2' RSS BHA modules as per Baker DD instructions." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 39m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Plugged into tools and verified same. Meanwhile cleared rig floor from casing equipment." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 39m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Made PA announcement and raised barriers. Installed RA sources." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 129m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: P/U and M/U 5' HWDP and jar. RIH to 129 m. Installed totco ring." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1045m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Installed PS21 slips. RIH w/ 8 1/2' RSS BHA on 5 1/2' DP from 129 m to 1045 m. Avg. tripping speed 610 m/hr." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1045m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Filled pipe and performed choke drill with both crews." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1045m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Performed shallow test on downhole tools as per Baker instructions." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1946m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH w/ 8 1/2' RSS BHA on 5 1/2' DP from 1045 m to 1946 m. Avg. tripping speed 724 m/hr." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1946m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: M/U TDS and filled pipe. Tested downhole tools as per Baker instructions." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH w/ 8 1/2' RSS BHA on 5 1/2' DP from 1946 m to 2914 m. Avg. tripping speed 775 m/hr." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: M/U TDS and filled pipe. Meanwhile performed TBT for slip & cut." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Pressure tested annular BOP to 20/150 bar for 5/10 min." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- other' and lasted for 3.2 hours. Operational details: Rigged up, slipped and cut 48 m drill line. Cleaned and cleared rig floor." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Calibrated block height with rig and Baker sensors." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2954m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH on 5 1/2' DP from 2914 m to 2954 m. Took up/down weights." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3015m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Washed down from 2954 m to 3015 m w/ 500 l/min. Tagged TOC/LC at 3015 m." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3015m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Increased flow rate to 2400 l/min, 244 bar. Downlinked as per Baker instructions. Commenced increasing MW to 1,34 sg." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled plugs and LC from 3015 m to 3017 m. WOB 1 - 6 MT. 2400 l/min/ 244 bar. 80 rpm / 12 - 13 kNm." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3046m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled cement from 3017 m to 3046 m. WOB 0 - 9 MT. 2400 l/min/ 244 bar. 80 rpm / 10 - 14 kNm. Soft cement from 3018 - 3030 m. Firm cement from 3030 - 3046 m" "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled out shoe at 3047 m. Drilled and cleaned rat hole from 3047 m to 3056 m. WOB 0 - 10 MT. 2200 l/min/ 220 bar. 80 - 90 rpm / 10 - 18 kNm. Wiped area every 1,5 m." "On 2014-03-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 3 m new formation to 3059 m." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Reamed from 3059 m back into shoe 3047 m w/ 2200 l/min/ 210 bar, 80 RPM / 10 - 12 kNm. Reamed area 2 times. Pulled into 9 5/8' shoe without rotation, packed off at 3048 m. Run back down and established rotation. Reamed area. Pulled into shoe without rotation, ok." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Circulated and cond. mud w/ 2300 l/min/ 200 bar, 30 RPM / 10 kNm, ECD 1,48 SG. Meanwhile performed TBT for FIT." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Spaced out string and closed UPR. Lined up to pump down DP and annulus." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: Attempted several times to test line-up to 120 bar, w/o success. Flushed through lines. Tested cement unit, greased bleed off valve and checked both kill and standpipe manifold line-up. Performed line test to 120 bar." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Performed FIT to 1,60 SG EMW using 1,34 SG mud. Pumped 530 ltr from 10 bar to 76 bar at cement unit w/ 90 l/min. Bled back 481 ltr. (MWD sensor data: 451,3 bar, 2856,1 m TVD, 1,61, sg EMW)" "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Opened BOP and lined manifolds up for drilling." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3040m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Established circulation and sent downlink. RIH to bottom and circulated with 2200 l/min. Baker performed diagnostics on downhole tools. Pulled into 9 5/8' shoe and continued troubleshooting on AutoTrak RSS. Decided to POOH and change AutoTrak RSS." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3033m. The activity was categorized as 'drilling -- survey' and lasted for 2.2 hours. Operational details: Scientific prepared and programmed drop gyro tool. Meanwhile circulated w/ 2450 l/min , 230 bar. Performed diagnostic downlinks as per Baker instructions. POOH from 3040 m to 3033 m. B/O TDS." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3033m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: P/U and dropped gyro. M/U TDS and pumped gyro down with 600 l/min, 23 bar as per Scientific instructions." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3033m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Flowchecked well, well stable." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3033m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Pumped 4m3 1,63 sg slug and chased same." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3033m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Waited on gyro survey as per Scientific instructions." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2680m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: POOH w/ 8 1/2' RSS BHA on 5 1/2' DP from 3033 m to 2680 m." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2680m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took gyro surveys as per Scientific instructions." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2551m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: POOH from 2680 m to 2551 m." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH from 2551 m to 2632 m, taking gyro surveys as per Scientific instructions." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1427m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: POOH w/ 8 1/2' BHA on 5 1/2' DP from 2632 m to 1427 m." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1427m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took gyro surveys as per Scientific instructions." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 341m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: POOH w/ 8 1/2' BHA on 5 1/2' DP from 1427 m to 341 m. Avr. tripping speed 1086 m/hr." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 341m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: M/U TDS and performed rotational gyro surveys as per Scientific instructions." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 143m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: POOH from 341 m to 143 m." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 143m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Flowchecked well, well stable. Meanwhile performed TBT for handling BHA." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 143m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed to 5' handling equipment." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 38m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: POOH 8 1/2' BHA. Racked 5' HWDP, recovered gyro. L/O jar on HTS." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 38m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Held TBT, errected barriers and made PA announcement." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 24m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Removed RA sources." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 24m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Plugged into tools, downloaded data and performed fault finding." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 24m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for using rig tongs to B/O bit and AutoTrak RSS." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: POOH to surface. B/O bit using rig tongs. B/O AutoTrak using IRN, L/D same." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: P/U new steering head and M/U to BHA. M/U bit using rig tongs." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Plugged into tools and verified same." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installing RA sources. Raised barriers and made PA announcement." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Installed RA sources." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: RIH with 8 1/2' 5' HWDP stands from derrick to 140 m. P/U jar from HTS." "On 2014-03-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed elevator inserts to 5 1/2'." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U first 5 1/2' DP stand, M/U to BHA. Installed PS 21 slips." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1018m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH w/ 8 1/2' RSS BHA on 5 1/2' DP from 140 m to 1018 m. Avg. tripping speed 878 m/hr." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1018m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: M/U TDS. Filled string w/ 800 l/min. Increased flow to 2200 l/min, 148 bar and shallow tested tools as per Baker instructions." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2030m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: RIH w/ 8 1/2' BHA on 5 1/2' DP from 1018 m to 2030 m. Avg. tripping speed 690 m/hr." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2030m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: M/U TDS and filled pipe. B/O TDS." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3035m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: RIH w/ 8 1/2' RSS BHA on 5 1/2' DP from 2030 m to 3035 m. Avg. tripping speed 804 m/hr." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3059m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Established circulation at 9 5/8' shoe. Washed down to bottom from 3035 m to 3059 m w/ 2200 l/min/ 205 bar, 60 RPM / 11 kNm, 1,50 sg ECD." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3072m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 8 1/2' hole from 3059 m to 3072 m. Avg. ROP: 5,7 m/hr. WOB 3 - 9 MT. 2200 l/min/ 206 bar. 100 rpm / 12 - 15 kNm. ECD 1,50 sg. Downlinked as per Baker DD instructions." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3072m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Downlinked to ribs off. POOH from 3072 m to 3042 m into 9 5/8' shoe. Took SCRs." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3042m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot decoding from downhole tools. Adjusted flow rates as per Baker instructions. Meanwhile investigated faulty drawworks motor." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3072m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Downlinked to ribs on. RIH to bottom at 3072 m." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3170m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3072 m to 3170 m. Avg. ROP: 14 m/hr. WOB 3 - 8 MT. 2200 - 2400 l/min/ 195 - 220 bar. 100 - 160 rpm / 12 - 23 kNm. ECD 1,50 - 1,53 sg." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3170m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Flowchecked well on T/T. Well stable. Took SCRs." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3235m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled and oriented 8 1/2' hole from 3170 m to 3235 m. Avg. ROP: 20 m/hr. WOB 2 - 6 MT. 2400 - 2100 l/min/ 225 - 185 bar. 160 rpm / 12 - 22 kNm. ECD 1,53 - 1,50 sg. Max gas: 2,8 % from 3208 m lag depth." "On 2014-03-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3290m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3235 m to 3290 m. Avg. ROP: 18,3 m/hr. WOB 4 - 6 MT. 2100 l/min/ 180 bar. 150 rpm / 12 - 20 kNm. ECD 1,50 sg. Max gas: 2,8 % from 3235 m lag depth." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3356m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3290 m to 3356 m. Avg. ROP: 18,9 m/hr. WOB 4 - 8 MT. 2150 l/min/ 190 - 200 bar. 150 rpm / 12 - 20 kNm. ECD 1,52 sg." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3356m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCRs." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3396m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3356 m to 3396 m. Avg. ROP: 26,6 m/hr. WOB 5 - 9 MT. 2150 l/min/ 190 - 200 bar. 150 rpm / 12 - 20 kNm. ECD 1,52 sg." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3396m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Re-took survey on connection." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3429m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3396 m to 3429 m. Avg. ROP: 22 m/hr. WOB 3 - 6 MT. 2150 l/min/ 190 - 195 bar. 150 rpm / 14 - 18 kNm. ECD 1,52 sg." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3639m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3429 m to 3639 m. Avg. ROP: 22 m/hr. WOB 2 - 5 MT. 2150 l/min/ 190 - 195 bar. 150 rpm / 10 - 20 kNm. ECD 1,50 - 1,51 sg. Max gas: 4,7 % from 3615 m lag depth." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3639m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCRs." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3639 m to 3695 m. Avg. ROP: 24,9 m/hr. WOB 3 - 7 MT. 2150 l/min/ 195 - 198 bar. 120 - 150 rpm / 15 - 19 kNm. ECD 1,50 - 1,51 sg. Max gas: 4,0 % from 3649 m lag depth." "On 2014-03-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3806m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3695 m to 3806 m. Avg. ROP: 22,2 m/hr. WOB 4 - 10 MT. 2150 l/min/ 195 - 198 bar. 150 rpm / 15 - 20 kNm. ECD 1,49 - 1,51 sg. Max gas: 6,0 % from 3774 m lag depth." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3840m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3806 m to 3840 m. Avg. ROP: 27,2 m/hr. WOB 3 - 8 MT. 2150 l/min/ 195 - 198 bar. 150 rpm / 15 - 20 kNm. ECD 1,49 - 1,50 sg. Max gas: 4,8 % from 3825 m lag depth." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3840m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Reamed single twice, tared CoPilot as per Baker instructions." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3880m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3840 m to 3880 m. Avg. ROP: 16 m/hr. WOB 6 - 10 MT. 2150 l/min/ 196 - 200 bar. 150 rpm / 15 - 22 kNm. ECD 1,51 sg. Max gas: 4,5 % from 3856 m lag depth." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3880m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCRs." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3903m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3880 m to 3903 m. Avg. ROP: 10,3 m/hr. WOB 8 - 10 MT. 2150 l/min/ 200 bar. 150 - 90 rpm / 15 - 22 kNm. ECD 1,51 sg. Max gas: 3,6 % from 3869 m lag depth. Reduced RPM to 90 while driilling hard stringers in interval." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4009m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and geosteered 8 1/2' hole from 3903 m to 4009 m. Avg. ROP: 21,2 m/hr. WOB 5 - 12 MT. 2150 l/min/ 195 - 208 bar. 150 - 90 rpm / 15 - 22 kNm. ECD 1,52 sg. Max gas: 3,7 % from 3979 m lag depth. Reduced RPM to 90 while driilling hard stringers in interval." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled and geosteered 8 1/2' hole from 4009 m to TD at 4094 m. Avg. ROP: 21,3 m/hr. WOB 5 - 10 MT. 2150 l/min/ 200 - 208 bar. 150 rpm / 15 - 22 kNm. ECD 1,52 sg." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated hole clean w/ 2200 - 2400 l/min/ 205 - 230 bar, 150 - 160 RPM / 12 - 16 kNm, ECD 1,51 sg. Racked back one stand and reciprocated string while circ." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4050m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Stopped rotation. Performed pipe stretch calibration and re-logging passes as per Baker instructions. Circulated with 2400 l/min/ 235 bar." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4050m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated hole clean w/ 2400 l/min/ 230 bar, 160 RPM / 12 - 16 kNm, ECD 1,52 sg. Circulated in total 3 B/U. Reciprocated string while circ." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4075m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Flowchecked well, well stable. Took up/down weights and torque readings." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Performed sticky test with BHA partly across reservoir sands, 5 MT overpull. Performed second test with full BHA across reservoir, 10 MT overpull." "On 2014-03-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3856m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: Took pressure points as per Geology/Baker instructions. Positioned string on depth, sent downlink and activitated TesTrak sequence. Circulated with 1900 l/min while taking pressure points. Took 4 points at following bit depths: # 1: 4010 m MD # 2: 3958 m MD # 3: 3891 m MD # 4: 3856 m MD" "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3306m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.8 hours. Operational details: Took pressure points as per Geology/Baker instructions. Positioned string on depth, sent downlink and activitated TesTrak sequence. Circulated with 1900 l/min while taking pressure points. Took 9 points at following bit depths (in total 13 points): # 5: 3801,4 m MD # 6: 3773,4 m MD # 7: 3753,4 m MD # 8: 3653,4 m MD # 9: 3636,4 m MD # 10: 3584,4 m MD # 11: 3556,4 m MD # 12: 3526,4 m MD # 13: 3306,4 m MD" "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH w/ 8 1/2' RSS BHA on 5 1/2' DP from 3306 m to 3040 m into the 9 5/8' shoe. Pulled wet." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well. Took up/down weights and torque readings." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped slug and dropped 3' drift." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 736m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: POOH w/ 8 1/2' RSS BHA on 5 1/2' DP from 3040 m to 736 m. Avg. tripping speed 709 m/hr." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 736m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned windows for driller and PRS operator. Filled T/T." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH on 5 1/2' DP from 736 m to 143 m. Avg. tripping speed 593 m/hr." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well prior to pulling BHA through BOP, well stable. Meanwhile changed from PS21 slips to master bushings." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 102m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH and R/B last stand 5 1/2' DP. Changed elevator inserts to 5'." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: L/D 5' HWDPs and jar." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held TBT, raised barriers and made PA announcement. Removed RA sources." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Plugged into tools and downloaded data. Meanwhile R/D bypass actuator unit." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: L/O 8 1/2' BHA modules as per Baker DD instructions." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor. Inspected TDS for PDOs." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT prior to picking up 7' liner hanger and R/B same." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: P/U 7' liner hanger from HTS. Set same in rotary and installed 6 m DP pup joint. POOH hanger, cleaned and R/B same in aft PRS." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for R/U casing equipment." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: R/U handling equipment for 7' liner." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for running 7' liner." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 59m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U 7' reamer shoe joint. M/U shoe joint, 3 x intermediate joints and float/landing collar joint and RIH to 59 m. Tested shoe float holding," "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 59m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Filled liner and checked for flow through. Observed FC/LC not draining." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 59m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Installed swedge and verified circulation. L/D swedge." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 71m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 7' liner from 59 m to 71 m." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 71m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Drawworks shut down due to cooling water alarm. Troubleshot cooling water pump." "On 2014-03-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 7' 29 ppf 13CrS110 VamTop HT liner from 71 m to 110 m. Filled liner every 5th joint. Average running rate 6 joints/hr. Installed pup joint 'Q' as per tally." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 263m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 7' 29 ppf 13CrS110 VamTop HT liner from 110 m to 263 m. Filled liner every 5th joint. Average running rate 6,5 joints/hr." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 427m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 7' 29 ppf 13CrS110 VamTop HT liner from 263 m to 427 m. Filled liner every 5th joint. Average running rate 7 joints/hr." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 668m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 7' 29 ppf 13CrS110 VamTop HT liner from 427 m to 668 m. Filled liner every 5th joint. Average running rate 7 joints/hr. Installed pup 'K' as per tally." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 668m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT with day shift." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1149m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: RIH with 7' 29 ppf 13CrS110 VamTop HT liner from 668 m to 1149 m. Filled liner every 5th joint. Average running rate 7,4 joints/hr. Installed pup 'O' as per tally." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1149m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Removed FMS slips and installed master bushings. Changed elevator inserts to 5 1/2'." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1149m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for installing 7' liner hanger. Counted remaining joints on deck prior installing hanger." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1149m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Transfered liner hanger assy from aft PRS to TDS. Installed wiper plugs as per Weatherford instructions. M/U hanger." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1149m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed protection from hanger. Weatherford liner operator checked set screws. RIH hanger below rotary." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1149m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: R/D Weatherford tong and cleared rig floor." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1190m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 7' liner on 5 1/2' HWDP stand from 1149 m to 1190 m. M/U TDS." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1190m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke circ. and increased flow in steps to 1000 l/min/ 40 bar. Circulated 1x liner volume." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1373m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 7' liner on 5 1/2' HWDP stands from 1190 to 1373 m. Filled string." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: RIH with 7' liner on 5 1/2' DP landing string from 1373 m to 3040 m inside the 9 5/8' shoe. Filled pipe every 5 stand. Avg. tripping speed 335 m/hr." "On 2014-03-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Broke circulation with 100 l/min. Increased flow in steps to 850 l/min/ 55 - 60 bar. Circulated one annulus volume prior to entering open hole." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated one annulus volume with 800 l/min 60 bar prior to entering open hole. Took up/down weights. Hanger shear limitation while RIH 64 bar." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3564m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 7' liner on 5 1/2' landing string from 3040 m to 3564 m. Filled pipe every 5 stand. Avg. tripping speed 330 m/hr. Encountered tight spots 3210 - 3230 m, 3270 m - 3310 m, 3390 m - 3460 m. Slided through spots with 10 -15 Mt, weight dropping off." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4036m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 7' liner on 5 1/2' landing string from 3564 m to 4036 m. Filled pipe every 5 stand." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4075m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Washed and worked w/ 7' liner on 5 1/2' landing string from 4036 m to 4075 m w/ 250 - 450 l/min/ 35 - 60 bar. Took weight and experienced pack-offs, pulled above restrictions to clear pack-off and worked string down. Prior to connection circulated stationary with 450 l/min, 55 bar." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4078m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made connection and established circulation. Washed/worked w/ string from 4075 m to 4078 m w/ 450 l/min/ 55 bar." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4079m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Established 20 rpm rotation. Reamed w/ 7' liner 4078 m to 4079 m w/ 500 l/min/ 55 bar. Experienced pack-off. Pulled above restriction." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4081m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Established circulation w/ reduced rate and reamed down from 4079 m to 4081 m w/ 300 l/min/ 40 bar. String rotation 20 rpm." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4084m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Reamed down w/ 20 rpm from 4081 m to 4084 m and increased flow to 440 l/min/ 45 bar." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Worked liner down with 20 MT from 4084 m to 4087 m w/o flow and rotation." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Established circ. in steps to 500 l/min, 54 bar. Attempted to establish rotation, pressure spike triggered pump elec. pop-offs at 64 bar. Established circ. in steps to 700 l/min, 61 bar. Circulated until stable pressure, decreased flow rate to 500 l/min, 48 bar and established rotation with 10 rpm, 23 kNm. Increased to 20 rpm, 18 - 21 kNm." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4090m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Reamed down w/ 7' liner from 4087 m to 4090 m w/ 500 l/min/ 40 bar, 20 rpm, 18-21 kNm." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4090m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Decision made to set liner at 4087 m. Continued circ. w/ 500 l/min/ 48 bar, 20 rpm, 18-21 kNm. Meanwhile prepared new space out and located pup joints." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4075m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Stopped rotation and circ. POOH to 4075 m and set back DP stand. P/U and M/U 3 m and 4,5 m DP pup joint." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4075m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U and M/U cement head. Installed hose and control lines." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Washed in w/ 7' liner on landing string from 4075 m to 4087 m w/ 400 l/min/ 48 bar. Positioned hanger at setting depth." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Increased flow in steps to 800 l/min/ 80 bar. Established rotation with 20 rpm, 17 - 20 kNm. Circulated 1 x B/U. Observed cement head swivel leaking while rotating. Stopped rotation. Performed TBT for cement job while circulating." "On 2014-03-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Dropped ball. Circulated down ball at 200 l/min. Landed ball in liner hanger ball seat. Pressured up to 170 bar and set liner hanger." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Verified hanger set by applying 30 MT. Released hanger RT as per Weatherford instructions. Increased pressure to 210 bar to shear out ball seat." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Increased flow in steps to 1500 l/min/ 176 bar. Reduced rate to 1100 l/min, 155 bar after observing slight loss tendency. Verified rotation with 20 rpm, swivel still leaking. Stopped rotation." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped 15 m3 of 1,56 sg spacer w/700 l/min/ 83 - 58 bar. Isolated rig pumps from cement line, lined up and applied 30 bar against IBOP with rig pumps." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Lined up through cement hose and verified line-up. Dropped dart # 1 for bottom plug. Mixed and pumped 18,4 m3 1,90 sg cement slurry w/ 650 l/min. Pumped 890 l drill water after cement job. Rotated liner while pumping cement, stoped rotation due to leaking swivel. Released dart # 2 for top plug. Displaced cement with 900 l/min. Slowed down to 700 l/min prior to first dart releasing bottom WP at 570 strokes, 61 bar SPP. Continued pumping with 900 l/min/ 35 - 96 bar. Reduced pump rate at 1350 strokes to 700 l/min/ 67 bar. Observed second dart releasing top WP. Continued displacement with 1000 l/min. Established liner rotation with 20 rpm prior to cement entering the annulus. Lowered rate to 800 l/min after experiencing potential loss indications. Slowed down to 500 l/min on the last 2 m3. Bumped the plug after 2430 strokes / 52,7 m3, 95 % pump efficiency, 120 bar. No losses to the formation." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Increased pressure to 190 bar with rig pumps. Equalized with cement unit and pressure tested liner to 300 bar/ 10 min." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed cement hose and checked for back flow. Floats holding." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2927m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pulled running tool up and packer actuator dogs above PBR. Applied 40 MT to set liner TSP packer." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2927m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up cement unit via kill manifold. Unable to obtain good line test to 320 bar. Decided to abort packer test." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2927m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: B/O and L/O cement head. Applied 30 bar to string, P/U 2m and observed pressure drop. Increased flow to 2000 l/min, 108 bar and circulated out excess cement while pulling out of PBR. Observed 18 MT overpull while POOH." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2927m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Racked double in fwd PRS. Installed sponge balls and circulated string clean w/ 2000 l/min/ 93 bar. Observed cement and interface in returns." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2778m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with 5 1/2' landing string from 2927 m to 2778 m. Pulled wet. Pumped slug." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2778m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U double with pups from PRS. M/U to string and B/O pup joints." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: POOH with 5 1/2' landing string/RT from 2778 m to 30 m. Avg. tripping speed 785 m/hr." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed PS21 slips and installed master bushings." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for laying out hanger RT." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Laid out running tool and 6 m pup joint." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor from excess equipment." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Serviced fwd and aft PRS." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed handling equipment from 5 1/2' to 3 1/2'." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TBT for P/U clean-out assy and 3 1/2' DP from deck." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: P/U and RIH 7' clean-up assembly #4 (mill, scraper, magnets). P/U and M/U first 3 1/2' DP single." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed to Odfjell slips and connected hoses. Discovered damaged connections on slips control panel." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 39m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: P/U and RIH with two 3 1/2' DP using manual slips. Meanwhile mechanic troubleshot on Odfjell slips." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 39m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Changed inserts and guides on PS21 slips to 3 1/2'. Installed slips. Installed shut off valve to isolate slips with low string weight." "On 2014-03-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 681m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.5 hours. Operational details: P/U singles while RIH w/ 7' clean-out assy on 3 1/2' DP from 39 m to 681 m. Avg. 20 joints/hr." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1090m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: P/U singles while RIH w/ 7' clean-out BHA on 3 1/2' DP from 681 m to 1090 m. Avg. 21,5 joints/hr." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1090m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1124m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: P/U and M/U clean-up assemblies #5 (tie back mill, well commisioner, magnet, drift), #6 (MFCT-HD, well patroler) and #7 (magnets). Surface tested tools as per MI Swaco SPS instructions." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1716m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH w/ 7' x 9 5/8' clean-out BHA on 5 1/2' DP from 1124 m to 1716 m. Avg. tripping speed 592 m/hr." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1716m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Scraped SafeLock plug setting area by reciprocating in interval from 624 to 647 m, rotating string with 40 RPM / 2 - 4 kNm and pumping w/ 1000 l/min/ 115 bar." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2529m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: RIH w/ 7' x 9 5/8' clean-out BHA on 5 1/2' DP to 2529 m. Filled string. Restricted speed." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2529m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation with 600 LPM/52 bar." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2529m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Closed UPR. Pressure tested Liner Packer to 20/300 bar for 5/10 min. Pumped 2600 ltr. Bled back 2570 ltr." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2529m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Opened UPR and dis connected TDS." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued to RIH w/ 7' x 9 5/8' clean-out BHA on 5 1/2' DP from 2529 to 2914 m. Restricted speed: 1 min/stand." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: M/U TDS, pulled pipe in tension and filled pipe." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Stopped pumping and recorded up/down weights: 147/125 T. Rotational weight at 20 RPM: 135 T / 7-8 kNm. Started pumps with 500 LPM/39 bar: Up/down weights: 140/131 T." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3411m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: RIH through Liner PBR at 2927 m with 29 RPM / 7-9 kNm. Pumped with 500 LPM/39 bar. No obstruction observed. Stopped rotation and flow. Continued RIH with scraper assy on 5 172' DP from 2914 to 3411 m." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3411m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Toolbox talk prior to P/u assy #8 and #9." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: P/U and M/U assy #8 (10 3/4' Scraper/drift) and #9 (Wellpatroller)" "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3965m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: RIH w/ 7' x 9 5/8' x 10 3/4' clean-out BHA on 5 1/2' DP from 3420 to 3965 m. Restricted speed: 1,5 min/stand." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3965m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: M/U TDS and filled pipe. Established 1000 LPM/145-155 bar and 50 RPM/8-13 kNm." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4012m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Scraped area at 2897 m +/- 15 m (3980 to 4012 m bit depth) with 1000 LPM/145-155 bar and 50 RPM/8-13 kNm." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Washed/reamed down from 4012 to 4025 m and tagged TOL with 2 T. TOL tagged at 2927 m." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Picked up 5 m and ran back to 4025 and polished PBR." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Picked up to 4019 m and circulated and conditioned mud with 1495 LPM/270 bar and 90 RPM/11-14 kNm." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Sheared MFCT with 25 T down weight and observed seal ring sheared at 15 T." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Confirmed MFCT open with 500 LPM/15 bar. Staged up pumps and circulated 3 x btms up with 3770 LPM/270 bar." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cycled MFCT to closed position. Sat packer on Well Commisoner with 15 T." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pressure tested Well Commisoner element to 70 bar for 10 min." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: Continued circulation while preparing for wash train and displacement." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flushed MP 2 and 3 and lines with Baseoil." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Pumped 0,84 SG Baseoil with 500 LPM. Initial pumping pressure 44 bar. FCP 100 bar SPP. Pumped 26,8 m3 / 1238 strokes of 0,84 SG Baseoil." "On 2014-03-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Monitored pressure for thermal effect." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Monitored well for thermal effect. None observed." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Recorded up/down weights: 162/130 T. Activated Well Commisoner element. Lined up to cement unit and pumped up to 110 bar for equalizing. Opened up valve between cement unit and manifold. SPP seen at rig system: 102 bar." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Bled off pressure at cement unit in 30 bars step. Bled off to 13,21 bar at cement unit / 7 bar SPP at rig system. Bled back 310 ltr." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Inflow tested the Liner and Liner Lap to 95 bar diff pressure. Pressure increased 2,7 bar in 30 min." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4025m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pressured up DP to 102 bar SPP using cement pump. Volume pumped: 530 ltr. Released Well Commisoner element. Closed valve to isolate cement pump. Rotated pipe with 10 RPM/13-13 kNm and pulled PBR polish mill 2 m above TOL" "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed Toolbox talk for displacing surface lines." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Splitted STP manifold to displace and clean surface lines. Displaced Choke and Kill lines, all Choke buffer tanks and Poorboy degasser / U-tube to Baseoil." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Monitored well on TT. Meanwhile cleaned rig floor from oil based mud." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Emptied Triptank of OBM and filled with Baseoil." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cleaned surface system and prepared for displacement job. Meanwhile cleaned and cleared in drilling areas." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Cleaned surface system and prepared for displacement job. Meanwhile cleaned and cleared in drilling areas." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Performed TBT for displacement." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Displaced well: Pumped 15 m3 of push pill with 1140 LPM/270 bar, 90 RPM/16 kNm. Pumped 39 m3 Soap pill with 2000-1900 LPM/240-280 bar and 90 RPM/12-16 kNm. Pumped 52 m3 1,03 SG NaCl Packer Fluid with 2226 LPM/230 bar and 90 RPM/12-17 kNm." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Recorded up/down weights: 178/137 T. Opened MFCT by setting down 12 T." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued to displace well to 1,03 SG NaCl Packer Fluid. Started with 500 LPM/30 bar and when MFCT was confirmed open, increased to 3960 LPM/132 bar and 90 RPM/11-17 kNm." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Closed MFCT." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pressure tested well against LPR to 345 bar for 10 min. 2400 ltr pumped / 2400 ltr in return." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flowchecked well - well static." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4019m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flushed/displaced Choke and Kill lines from Baseoil to 1,03 SG Packer Fluid." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3762m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: POOH dry with Scraper assy on 5 1/2' DP from 4019 to 3762 m while L/D drillpipe to deck. Restricted speed: 1,5 min/stand." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3762m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Observed baseoil on tooljoints. Circulated 15 m3 of 1,03 SG NaCl Packer Fluid. Clean Packer Fluid observed in return." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3618m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: POOH wet with Scraper assy on 5 1/2' DP from 3762 to 3618 m while L/D drillpipe to deck. Observed backflow from DP. Restricted speed: 1,5 min/stand." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3618m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Broke circulation with 500 LPM/10 bar and increased in steps up to 1770 LPM/130 bar. Confirmed MFCT closed." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3618m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Observed overflow from pipe. Pumped 10 m3 of 1,04 SG NaCl Packer Fluid and further another 10 m3 of same." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3441m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: POOH wet with Scraper assy on 5 1/2' DP from 3618 to 3441 m while L/D drillpipe to deck. Observed backflow from DP. 5,3 m3 lost from start trip. Restricted speed: 1,5 min/stand." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3441m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: L/D Wellpatroler and Razor back. Inspected same. L/D on rigfloor due to wind limiatations." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3441m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flowchecked well - well static. Meanwhile checked cleaning tools. Well Patroller 80 % full." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3331m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: POOH wet with Scraper assy on 5 1/2' DP from 3441 to 3331 m while L/D drillpipe to deck. Observed backflow from DP. Total 8 m3 lost Packer Fluid from start of trip. Restricted speed: 1,5 min/stand. Bursted hose on IRN." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3331m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Replaced hydraulic hose on aft AR. Meanwhile bundled 3 1/2' DP on deck and installed protectors on 5 1/2' DP. Removed Well Patroler and Posi drift assemblies from rig floor." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3331m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held TBT prior to POOH and L/D pipe." "On 2014-03-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2521m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: POOH with Scraper assy on 5 1/2' DP from 3331 to 2521 m while L/D drillpipe to deck. Restricted speed: 1,5 min/stand until TOL at 2927 m." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1138m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.8 hours. Operational details: Continued POOH with Scraper assy on 5 1/2' DP from 2521 to 1138 m while L/D drillpipe to deck." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1340m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: RIH with scraper assy on 5 stands of 5 1/2' DP from derrick 1138 to 1340 m." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1340m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: P/U single from deck and B/O XO and L/D same." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2106m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Continued RIH with scraper assy on further 19 stands of 5 1/2' DP from derrick from 1340 to 2106 m." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1871m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued POOH with Scraper assy on 5 1/2' DP from 2106 to 1871 m while L/D drillpipe to deck." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1487m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Continued POOH with Scraper assy on 5 1/2' DP from 1871 to 1487 m while L/D drillpipe to deck. HTS belt failed." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1487m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Prepared for and changed out belt on HTS." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1138m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued POOH with Scraper assy on 5 1/2' DP from 1487 to 1138 m while L/D drillpipe to deck." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1138m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed Masterbushing. Changed out inserts from 5 1/2' to 3 1/2'." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1138m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flowchecked - well static." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1092m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: L/D single DP and cleaning assemblies from 1138 to 1092 m." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1092m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed Masterbushing and installed PS21 slips. Function tested same." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1092m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held TBT to discuss method for racking 3 1/2' DP in derrick." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 891m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: POOH with scraper assy on 3 1/2' DP from 1092 to 891 m. Racked stands in derrick. Replaced jaws in aft PRS and while continued operation with forward PRS." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 891m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed TOFS and held TBT for laying out 3 1/2' DP." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1092m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with Scraper assy on 3 1/2' DP from derrick from 891 to 1092 m." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 5.0 hours. Operational details: POOH with Scraper assy on 3 1/2' DP from 1092 to 10 m while L/D pipe to deck. Average speed: 216 m/hr" "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Inspected and L/D Magno assy to deck." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed PS21" "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Serviced TDS and checked Standpipe clamps in derrick. Serviced pipehandling equipment." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 53m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held TBT. P/U WH/BOP cleaning assy and RIH to 53 m." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 53m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Jetted slick joint and BOP with 1600 LPM/9 bar and 20 RPM/2 kNm." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 53m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Functioned BOP rams and annular." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 53m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Jetted slick joint and BOP with 1600 LPM/9 bar and 20 RPM/2 kNm." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 73m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Picked up and ran Riser brush" "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 183m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Washed in from 73 to 183 m with 3500 LPM/65 bar and 20 RMP/4kNm." "On 2014-03-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 188m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: RIH and tagged WB with 2 T with assy 3 (Magnosweep) at 139 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 73m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: POOH with BOP cleaning assy on 5 1/2' DP from 188 to 73 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled cleaning BHA and inspected same. L/D to deck. No debris on magnets and in Well Protector observed. Cleaned and cleared rigfloor." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: P/U Safelock assy from deck. Removed protection and clamp." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 210m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: RIH with Safelock assy on 5 stands of HWDP from 7 to 210 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 640m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: RIH with Safelock assy on 5 1/2' DP from 210 to 640m. Restricted speed: 1 min/stand." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 640m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Recorded up down weights: 97/95 T. Washed setting area with 1100 LPM/2 bar for 10 min while reciprocating string between 640 and 644 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 642m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Sat plug with mid element at 641,2 m according to procedures. Function tested ball valve." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 642m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Pressure tested plug from below to 345 bar for 10 min. Volume pumped/bled off from 10 bar: 1800/1700 ltr." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 638m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Closed ball valve according to procedure. Released RT. Pulled above Safelock plug." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 638m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Pumped 5 m3 HiVis pill above Safelock plug. Spotted same with 1,03 SG Packer Fluid with 2000 LPM/10 bar and 60 RPM/4 kNm." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 210m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: POOH with Safelock RT on 5 1/2' DP from 638 to 210 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: POOH with Safelock RT on 5 1/2' HWDP from 210 to surface." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Closed shear ram. Pressure tested well above Safelock plug to 345 bar for 10 min. Volume pumped/bled off from 10 bar: 835/835 ltr. Meanwhile inspected and L/D Safelock RT. Opened Shear ram." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 53m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: M/U Jetsub, 1 stand of 5 1/2' HWDP and WB RT" "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH with Jetsub/WB RT from 53 to 138 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Jetted WH area with 1500 LPM/5 bar." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 185m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH with Jetsub/WB RT from 138 to 185 m. Landed out in profile with 7 T down and pulled WB with 40 T overpull." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH with Jetsub/WB from 185 to 138 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Jetted WH area with 1500 LPM/6 bar." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with Jetsub/WB from 138 m to surface." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: L/O Wearbushing. Redressed WB RT." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held TBT." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and RIH PADRT with Lockdown sub to 139 m." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed Lockdown sub with 4 172 CW turns and 7 T down." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Increased pressure in 35 bars steps to 207 bar for setting and locking Lockdown sub. Kept pressure for 10 min." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Verified Lockdown sat by applying 30 T overpull." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: POOH with PADRT from 139 m to surface. Cleaned and cleared rig floor." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held TBT prior to nippling down BOP." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Rigged up Diverter chains and bridle. Removed Master bushing. Pumped out water from Diverter and Overshot. Bled down Overshot and removed control hose." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed Diverter and Slipjoint and sat back same. Production shut-down at 13:00 hrs." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Removed BOP Tensioners. Pumped out water from BOP. Disconnected NT2 and sat back BOP. Manwhile rigged down Diverter chains. Installed elevator and P/U Claxton XO and single of DP." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held TBT. Removed Master bushing. Lowered and stabbed Claxton tool to Riser. Transferred 127 T weight to Block." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed horizontal Tensioners and Moonpool scaffolding." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held TBT. Removed split hatches and commenced lowering tension on Cylinders and transferring load to Block. Notified Production to start up wells at 18:07 hrs. Meanwhile serviced TDS and changed encoder on Drawwork." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Rigged down Tension ring assembly." "On 2014-03-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waited on Weather window (12 hrs) for disconnecting and pulling HPDR. Meanwhile performed maintenance and started to change out wire on aft PRS." "On 2014-03-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on Weather window (12 hrs) for disconnecting and pulling HPDR. Meanwhile performed maintenance jobs and continued to change out wire on aft PRS. Installed 2 guidewires." "On 2014-03-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Waited on Weather window (12 hrs) for disconnecting and pulling HPDR. Meanwhile performed maintenance jobs and pressure tested BOP and manifolds to 20/345bar 5/10min. Spotted Well Partner equipment on rig floor." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.2 hours. Operational details: Waited on Weather window (12 hrs) for disconnecting and pulling HPDR. Meanwhile performed maintenance jobs and pressure tested manifolds to 20/345bar 5/10min. Rigged up hot stab sheaves in moonpool. Advised Production to shut down at 05:43 hrs." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: Held TBT. Ran Hot Stab and flushed same. Removed dummy stab and inserted minireel stab." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 127m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Production shut-in at 07:22 hrs. Disconnected HPDR. 130 T up weight." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 127m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: ROV installed debris cap and retrieved VX gasket. Meanwhile L/O XO and single DP." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 125m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pulled riser above RKB. Splitted and installed Spider. Function tested same." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 125m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed C-plate and Side door Elevator. Landed riser." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 120m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Broke BOP joint connection." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 120m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: L/O BOP joint to deck." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 120m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed BX-elevator and rotator." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH Tension joint." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Broke Tension joint connection." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: L/D Tension joint to deck." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Changed out Side door elevator. Installed BX elevator and Riser handling sub." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 93m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH HPDR from 103 to 93 m." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 93m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Broke out Upper Pup joint connection. Crane Boom Tip swayed into fibre glass handrail at PRS walkway in derrick." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 93m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: TOFS: Banksman observed Crane Boom Tip swayed into fibreglass handrail at PRS walkway in derrick. Stopped job. Barriered off area. Informed Supervisors, checked and secured fibre glass handrails." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 93m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: L/O Upper Pup joint to deck." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH Splash zone joint." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Started to break out connection on Splash zone joint." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held TBT for ongoing crew." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Continued to break out connection on Splash zone joint." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Deck crew on helideck." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Performed Crane Boom Tip inspection" "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Brought up 3 ea Riser lifting tools and slings to rig floor." "On 2014-03-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 35m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Continued to pull, break out and L/D HPDR joints from 79 to 35 m." "On 2014-03-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 12m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Continued pulling HPDR from 35 to 12 m." "On 2014-03-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: Due to limited deckspace, waited for loading a riser basket from boat and emptying it. Problems with Port crane occured." "On 2014-03-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 12.5 hours. Operational details: Waited on Crane repair: Trouble shot problem with fluctating pressure on Port Crane emergency brake. Started to change out pump. Hoisted Tension joint above RKB. Closed spider and secured C-plates on top. Informed Production to start up at 13:00 hrs. Meanwhile pressure tested TDS auto/man IBOP and Kelly hose to 20/345 bar for 5/10 min. M/U RT for Production Riser to std and racked in derrick. Performed maintenance and derrick inspection." "On 2014-03-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held TBT and installed Guide Funnel using Aft crane." "On 2014-03-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.2 hours. Operational details: Continued changing out pump on Port crane. Further cleaned oil system and changed oil. Meanwhile ROV cleaned and installed VX gasket and Debris cap. Continued to perform maintenance on drilling equipment." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 11.0 hours. Operational details: Waited on crane repair. Meanwhile performed maintenance including 5 yearly on choke manifold valve C7. Assisted on crane repair." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Prepared deck and removed Production Riser from basket to deck." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: L/O HPDR Tension joint. Removed RT and prepared same for backload." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lowered Guide base clamp to WH through RT." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Prepared cutting gear while Crane worked boat. Placed cutting gear on lower deck. Cleaned and cleared on rig floor and performed maintenance." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held TBT. P/U Procuction TBC to well center and retracted same. P/U Hotstab from Moonpool to rig floor. Flushed through Hotstab and inserted into TBC. Function tested TBC." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waited while deck personnel handled shuttle helicopter." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Placed double Production Riser on Catwalk. Worked on Claxton tool on deck. M/U lifting tool to double on Catwalk." "On 2014-03-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on weather window for running Production Riser." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 10.0 hours. Operational details: Waited on weather window for running Production Riser. Meanwhile cleaned and cleared in drilling areas, and performed PMs. Production advised to shut-down at 09:00 hrs." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held TBT for all involved personnel for running of Production Riser." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waiting on weather / Production shut down." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Ran Production Riser as per tally to 30 m. Tested each connection to 207 bar for 5 min." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Attached Guide wires to clamp on Riser. Ran wires to template and established by ROV assistance." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 38m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Ran double Production Riser from 30 to 38 m (second double) and tested connection to 207 bar for 5 min. Problems with port Crane occured." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 38m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Changed out solenoid valve on port Crane brake system." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 66m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran double Production Riser from 38 to 66 m (third double) and tested connection to 207 bar for 5 min." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 66m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Deck crew performed TOFS and evaluated use of port Crane due to earlier equipment failures." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 66m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed handover meeting for new arrived shift." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 66m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for running Production Riser." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 66m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waited due to deck personnel handling shuttle helicopter." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 95m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Ran double Production Riser from 66 to 95 m (fourth double) and tested connection to 207 bar for 5 min. Tested connection in middle of double to 207 bar for 5 min." "On 2014-03-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 95m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: P/U upper pup Riser joint and M/U same." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 102m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran Production Riser from 95 to 102 m. P/U Tension joint to Catwalk. Broke coupling on Elevator." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 102m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed coupling on Elevator." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Continued P/U Tension joint from Catwalk, made up and tested connection. Ran same and landed off on Landing plate on spider. P/U stand of 5 1/2' DP and flanged XO. M/U flanged connection to Tension joint and connected DP to TDS." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lifted Riser String and removed Landing plate. ROV removed Dust cap." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lowered very carefully Production Riser on landing string. Closed spider for guiding. Continued running until just above Guide Funnel." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held TBT for landing." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Stabbed Riser over Well Head." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed Guide Funnel and spotted on Sea Bed." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed Guide wires." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 136m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran and flushed Hot stab from Moonpool." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Landed Production Riser with 15 T. Locked to WH. Performed 10 T overpull test. Production advised to start up wells at 08:04 hrs." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Confirmed line up from cement unit and filled Riser with Seawater." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed line test to 200 bar for 5 min." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pressure test of TBC and Production riser to 20/200 bar for 5/10 min. Pumped/bled off 408 ltr." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Bled off pressure and drained string to tension joint." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Flushed TBC. Meanwhile installed Boat collision stool and prepared for Tension ring installation." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Recovered hotstab, Guide wire and wire clap to Moonpool." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Installed hatches on F-6 and half moons on F-1. Installed Tension cylinder on ring." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed Riser centralizer in tension deck." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Transferred 36 T from TDS to tension ring." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Performed survey to verify cutting depth." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for cutting of Riser." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Rigged up cutting equipment on tension joint. Cut same. Distance cut to RKB: 21,07 m" "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Retrieved cut to drill floor. Removed Riser Spider and installed outer ring and Master bushing. Broke off cut and handling sub." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Started to dress off cut." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Dressing off cut at WH. Meanwhile performed TBT." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Dressing off cut at WH. Meanwhile cleared rig floor of Riser running equimpent. F11 & F12 depressurized at 19:51 hrs." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held TBT for running Multibowl." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U HP Riser joint and Claxton handling tool. M/U same to Multibowl." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed bushings." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Ran Multibowl through rotary." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed bushings and set in slips." "On 2014-03-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: M/U XO to Claxton tool and P/U and M/U one stand of 5 1/2' DP." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Oriented and landed Multibowl on top of Tension joint." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Energized seals and pressure tested same. P/U 5 T to ensure slips are locked. Meanwhile rigged up control line for Claxton tool and prepared for nippling job. F14 & F15 depressurized at 04:00 hrs. F11 & F12 already depressurized." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Adjusted scaffolding to access Claxton tool." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Disconnected and pulled Claxton tool. Covered off below BOP deck level. Broke off XO and racked stand in derrick. L/D Claxton tool. Worked on Multibowl. Meanwhile prepared for lifting BOP." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed annular valve." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Moved BOP to well center and nippled up same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Made up NT2 connector and installed Tension cylinders on BOP. Informed Production to start up wells at 08:07 hrs." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed Slick joint and Diverter." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed Outer ring and Master bushing. Rigged down Diverter chain. Installed Elevator and Rotator." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Torqued up bolts on Slick joint and energized Diverter seals." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Filled Riser and BOP with seawater." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleared rig floor of excess equipment." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: P/U BOP test tool and M/U same. RIH with Test tool to 20 m. Problems getting test on Test tool." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Performed line-up test to 345 bar for 5 min. Closed BOP and pressured up to perform Connector test. Leakage observed at Multibowl. Re-seated tool and tested again - negative." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH with Test tool from 20 m and L/O same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: P/U Bowl protector and RT. M/U same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: RIH with Bowl protector to 20 m and released Bowl protector from tool. POOH with RT. Bowl protector on RT. Performed three attempts to set Bowl protector." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 150m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U Jetting assy. RIH with same to 150 m." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 150m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pumped 15 m3 hiVis and displaced same with seawater at 2500 LPM/5 bar. Waited 10 min. Jetted area from 150 to 130 m with 3000 LPM/220 bar and 10 RPM/1-2 kNm." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 183m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued RIH with jetting assy from 150 to 183 m. Displaced well with 1,03 NaCl brine at 3000 LPM/17 bar and 10 RPM/1-2 kNm." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH from 183 m and L/O Jetting assy." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U Annulus inserts RT and RIH on DP to 142,42 m." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Latched onto Annulus inserts sleeve." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH from 140 m." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed sleeve from RT and L/O same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: P/U and M/U Bowl protecter retrieving tool." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH to 20 m and latched on bowl protector. POOH with same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed Bowl protector from RT and L/D same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held TBT prior to rigging up for running casing." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged up for running casing." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held TBT." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U Tie back adapter and inspected same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 10 3/4' Tie back to 107 m" "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U adjustable Sub assy and inspected same." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued RIH with 10 3/4' Tie back from 119 to 141 m." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U and M/U circulation swedge." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Backed out casing Hanger RT" "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: POOH with casing Hanger RT and racked in aft PRS." "On 2014-03-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Started to rig down casing handling equipment." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed elevator for pulling 10 3/4' Tieback." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Pulled and L/D 10 3/4' Tieback pups and joints." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 7.2 hours. Operational details: Waited for equipment. Meanwhile performed maintenance. Serviced drilling equipment. Washed down in drilling areas." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Held TBT for rigging down casing equipment." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Rigged down casing handling equipment. Rigged up for running DP." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Deck crew on helideck: Waited on crane." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: M/U Jetting assy" "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 145m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: RIH with Jetting assy on 5 1/2' DP to 145 m." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 145m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Waited while HiVis pill was prepared." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 145m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Pumped 15 m3 1,03 SG HiVis pill and jetted Tieback Adapter area with 3000 LPM/27 bar and 10 RPM/2 kNm." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 145m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: M/U BOP test tool and XO." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 178m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with Jetting assy/BOP test tool on 5 1/2' DP from 145 to 178 m." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 178m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Opened V/V on WH below test tool." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 178m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Confirmed line-up and performed line test to 345 bar for 5 min." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 178m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Tested BOP connector to 20/345 bar for 5/10 min." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 164m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH from 178 to 164 m. B/O BOP test tool and XO." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH with Jetting assy on DP from 164 m to surface." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: B/O Jetting sub." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: M/U Tieback Sleeve running tool." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RIH with Tieback sleeve RT on 5 1/2' DP to 139 m." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Landed out. Engaged threads and made 4 turns at 2,5 kNm. Made several attempts to catch last thread with torque up to 7 kNm." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH with Tieback sleeve RT on 5 1/2' DP from 139 m to surface. L/D RT." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 121m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U Jetting assy and RIH on 5 1/2' DP to 121 m." "On 2014-03-31, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 121m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Waited for equipment. Meanwhile performed daily checks and washed down in shaker room and Pump room. Performed maintenance." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 121m. The activity was categorized as 'interruption -- repair' and lasted for 9.0 hours. Operational details: Waited for equipment. Meanwhile performed daily checks and PMs. Washed down in Pump room, Sack store and Moonpool. Removed ROV equipment from Moonpool." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 121m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held TBT for displacement job" "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 121m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Filled pits with drill water." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 160m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Positioned string at 160 m and displaced to drill water with 2000 LPM/6 bar. Pumped 74 m3." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 40m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH from 160 to 40 m." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Strapped out last stand." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RIH to 20,52 m to set Bowl protector. Strapped out to confirm depth." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Assisted in rigging up downhole camera equipment on drill floor." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Held TBT" "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: RIH with camera on 5 1/2' DP to 139 m." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Positioned camera at 139 m. Circulated with 200 - 900 LPM and adjusted depth as instructed. Recorded condition of Subsea Hanger 11 1/4' OD 2 TPI threads" "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH with Camera on 5 1/2' DP from 139 m to surface." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Rigged down camera equipment and L/D same." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: M/U Bowl protector RT and RIH to 20,52 m. POOH with Bowl protector." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: L/D bowl protector and P/U Jetting sub." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 180m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH with Jetting assy on 5 1/2' DP to 180 m" "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 180m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Cleaned out pits due to limited available clean pits. Mixed new 1,03 SG NaCl brine. Meanwhile prepared for running Tieback string. Cleaned on drill floor and in shaker room." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 180m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held TBT" "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 180m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Displaced well from 180 m and up to 1,03 SC NaCl Packer Fluid." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH with Jetting assy from 180 m to surface. L/D Jetting sub." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Held TBT for R/U handling equipment for 10 3/4' Tieback and rigged up same." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Held TBT for casing running." "On 2014-04-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 15m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: P/U and RIH 10 3/4' Tieback Adapter and joint to 15 m. Checked Adapter." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Continued to RIH with 10 3/4' tie back from 15 to 107 m." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: P/U and inspected adjustable Sub assy. Removed guides in slips and RIH with assy to 119 m." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: P/U racked landing string and RIH to above landing point." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Landed tie back adapter and sat off weight. Visuallly inspected color marking seen at Annulus valve at multi bowl. Orange seen. Evaluated situation and pulled up and re-landed two times. Yellow color seen." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Attempted to spin in 10 3/4' tie back adapter by elevator, but no rotation seen at Annulus valve on Multi Bowl. Spinned 6 1/2 turns using casing tong and released CHRT. Pulled out stand with CHRT and racked in aft PRS." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Held TBT" "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Rigged down casing handling equipment and rigged up for DP." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 5m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: P/U and M/U 10 3/4' tie back adapter setting tool." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 70m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with 10 3/4' tie back adapter setting tool on 5 1/2' DP to 70 m." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with 10 3/4' tie back adapter setting tool on 5 1/2' DP from 70 to 138 m." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 145m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Engaged torque tool and M/U tie back string to 17,5 kNm. Confirmed correct land out of tie back. Torqued up from 17,5 kNm to 30 kNm." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH with torque tool from 145 m and L/D same." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Deck crew at heli deck. Cleaned and cleared drillfloor." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: M/U jet sub assy and adjustable sub setting tool." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with adjustable sub setting tool to 27 m." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Confirmed correct space out. Applied 140 bar on string, took 12-13 ton overpull. Bleed off pressure and maintained over pull. Set adjustable sub as per Drill Quip procedure while Vetco observed for casing hanger movement." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Attempted several times to POOH with adjustable setting tool with no success." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 27m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Brainstorm. Discussed problem with town." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Closed annular, applied 20 bar on annulus. Pulled tool free and up 2 m with no over pull." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 22m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Opened annular and released pressure while pulled up 3 m with 6-8 ton drag. Observed 15 ton over pull, slacked of weight." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 19m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Closed annular, applied 20 bar on annulus. Stripped out to 19 m with 3 ton over pull. Bleed off pressure and opened annular." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH with adjustable setting tool from 19 m to surface. Inspected tool and observed locking ring broken in 3 pieces." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to B/O and L/D adjustable setting tool." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: B/O and L/D adjustable setting tool." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U and M/U casing hanger running string." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: P/U and M/U casing hanger running string as per Vetco procedurer." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to pressure test tie back adapter." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed line test to 345 bar for 5 min." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressure tested tie back adapter to 345 bar for 10 min. 454 ltr pumped and recieved." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with landing string and L/D same." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U and run seal assembly." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: M/U seal assembly on running tool. Connected hydraulic lines." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with seal assembly and landed out at 20,6 m. Engaged dogs and took 10 ton over pull." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Set seal assembly, applied 345 bar for 10 min." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released seal assembly running tool. POOH with running tool and L/D same." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U R/T and installed secondary bowl protector in well head." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH with secondary bowl protector running tool and L/D same." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U VMB plug retrieving tool." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: P/U and M/U VMB plug retrieving tool and inspected same." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: RIH with VMB plug retrieving tool to 160 m." "On 2014-04-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Removed manual slips and bushing from rotary." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 160m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Installed auto slips in rotary." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 636m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: RIH with VMB plug retrieving tool from 160 m to 636 m." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 636m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Established circulation with 2500 lpm, 18 bar and displaced out Hi-vis pill." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 642m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Established circulation with 200 lpm, 1 bar. Wash down onto plug. Released plug as pr Archer procedure. RIH past setting depth to confirmed plug free from 634 m to 642 m." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: POOH with VMB plug from 642 m. Inspected plug and L/D same." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Pulled bowl protector from 20 m." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor for excess equipment." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Prepared for running completion string. Change out casing equipment from 10 3/4' to 7'." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: R/U for running 7' completion string." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Performed pre-job meeting with crew prior to run 7' completion string." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 40m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: P/U and M/U 7' Mule shoe 7' completion string. Inspected EVO plug and granite packer. RIH to 40 m." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 40m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Installed pipe rollers." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 242m. The activity was categorized as 'completion -- completion string' and lasted for 3.8 hours. Operational details: RIH with 7' completion string 29 ppf centralizer joints from 40 m to 242 m . Average 6 joints/hr." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 242m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: P/U and M/U assembly # 4 DHPG and terminated cable according to SLB procedure. Function tested gauge." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 381m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 242 m to 381 m . Average 6 joints/hr." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 381m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to run 7' completion string." "On 2014-04-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 738m. The activity was categorized as 'completion -- completion string' and lasted for 4.8 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 381 m to 738 m. Average 6 joints/hr." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 845m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 738 m to 845 m. Average 6 joints/hr." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 845m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Inspected and serviced slips, elevator and tubing tong." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1140m. The activity was categorized as 'completion -- completion string' and lasted for 4.2 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 845 m to 1140 m. Average 6 joints/hr." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1199m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 1140 m to 1199 m. Average 6 joints/hr." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1199m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to run 7' completion string." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1199m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Inspected and serviced slips, elevator and tubing tong." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2098m. The activity was categorized as 'completion -- completion string' and lasted for 11.2 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 1199 m to 2098 m. Average 6 joints/hr." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2098m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to run 7' completion string." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2440m. The activity was categorized as 'completion -- completion string' and lasted for 3.8 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 2098 m to 2440 m. Average 7 joints/hr. Counted number of tubing left on deck prior to P/U DHSV." "On 2014-04-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2440m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: P/U and M/U assembly # 5 DHSV. Terminated cable according to procedure." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2440m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Pressure tested line/connection to 520/345 bar." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2808m. The activity was categorized as 'completion -- completion string' and lasted for 4.5 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 2440 m to 2808 m. Average 7 joints/hr." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2867m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 2808 m to 2867 m. Average 5 joints/hr." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2867m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to run 7' completion string." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: RIH with 7' completion string 29 ppf slick joints from 2867 m to 2920 m. Average 4 joints/hr. Counted number of tubing left on deck prior to P/U landing string." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: P/U landing sting. M/U TDS to string. Took up/down weight, 186/149 ton." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to preform space out and enter PBR." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Broke circulation with 200 lpm, 0,2 bar. RIH with landing string, stopped pumping when increased observed on STDP. Bleed off pressure. Continued RIH and landed off at 2931 m. Sheared no-go with 8 ton." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Pulled back and L/O landing string." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Changed handling equipment." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rearrange sheaves for control line cables." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Rearrange sheaves to allow winch to be used to remove casing slips." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Removed casing slips from rotary and installed bushings." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2908m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: L/O joint # 20." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2908m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U and M/U tubing hanger." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2908m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Terminated control lines according to GE procedure." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2909m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed C plate and landed tubing hanger in C plate." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2909m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Pressure tested lines to 35 bar/5 min. 450 bar/10 min." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2909m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed communication collar and control lines according to GE procedure." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2909m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: L/O tubing hanger handling tool." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2909m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U tubing hanger running tool." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2909m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: M/U tubing hanger running tool." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2909m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Conected DHSV control lines to THRT and pressure tested to 520bar as per Baker procedure." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2912m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lowered hanger below rotary. Install inner bushings." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Rih with 7' liner/ HGR from 2915 to 2930.9m and land off hanger in well head. Stick up when Landed off 1.41m." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Verified correct land off by leak test through ports on multi-bowl." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Conducted 15 ton overpull to verify hanger lockdown." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested hanger seal to 35/345 bar. Good test." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Opened DHSV and dropped ball. Install Swedge." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Flushed surface line from Cmt Unit to Rig floor prior to line test. pressure tested surface line to 345 bar." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Filled string with brine. Started circlate with 150 lpm to pump down EVO ball." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pump to 70 bar and hold pressure for 5 min. Bleed off to 50 bar. Pumped 235 ltr , returned 41 ltr. Bleed down from 50 bar to 5 bar, 30 ltr back, (Function Test )." "On 2014-04-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Equalized downhole pressure." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Pressured up control line to open DHSV." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to setting packer and pressure testing same." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pressured up tubing to 275 bar to set production packer, 15 min. Pressure test tubing to 345 bar/30 min with CMT Unit. Monitored annulus at well head for flow. Vol 0-275 bar = 700 ltr, 275-345 bar = 190 ltr." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Bleed back to 280 bar and performed 30 min 70 bar DHSV inflow test." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Bleed back pressure to 10 bar and perform 10 min 270 bar DHSV inflow test." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Equalize pressure and open DHSV." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to pressure test production packer." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: R/U for pressure testing down annulus. Trouble shoot on kill test line. Blocked or plugged line." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Unplugged kill line. Line plugged at v v K16 valve. Cleaned out and flushed line." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lined up kill test line to cement unit. Pressure tested kill test line to 35/345 bar, 5/10 min. Test failed. Flushed line and prepared for re-testing of line." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to line up and pressure test multi bowl." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lined up and pressure tested multi bowl to 35/345 bar, 5/10 min. Ok test." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Leak tested production packer from above to 35/345 bar, 5/35 min. 1063 ltr pumped, 974 ltr recieved." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: R/D hose and B/O swedge." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2931m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: R/U Aker wire line equipment and M/U tool string for pulling 7' EVO plug." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2912m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: RIH with wire line tool, plug catcher." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2912m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Latched onto EVO plug @ 2912 m. Work free plug. Waited to allow element to relax." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.2 hours. Operational details: POOH with EVO plug on wire line. L/O EVO plug and tool string. R/D wire line." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Pressure tested tubing/liner to 35/345 bar, 5/30 min. 1370 ltr pumped, 1208 ltr recieved." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Released tubing hanger running tool and L/O same." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: R/D tubing equipment." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with crew prior to R/D and clear rig floor for completion equipment." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: R/D and cleared rig floor for completion equipment. Changed to 3 1/2' handling equipment." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: M/U 6 3/8' BPV to 3 1/2' DP. RIH and installed 6 3/8' BPV in well head at 20,6 m." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with BPV running tool and L/D same." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor for excess equipment prior to N/D BOP." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to R/U and N/D diverter and BOP." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: R/U chains and slings onto Bails for pulling diverter. Bleed down overshot packer." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled diverter and set back same. Secured diverter." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: N/D NT2 connector as per procedure." "On 2014-04-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed Weatherford casing tong and equipment from drillfloor." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: N/D BOP and parked same on BOP carrier. Started production as per yellow Simops." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to N/D high pressure riser." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: N/D high pressure riser and L/D same." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Started to terminate control lines." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Terminate control lines. Meanwhile break out 7' csg swedge and X-O. Repaired leak on forw PRS." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: Installed spacer spool. GE pressure tested between V-63 and BT seal to 35 bar. Slumburger checked electric lines. GE pressure tested void and control line exits to 30/345 bar, 5/10 min. Meanwhile perform pre-job meeting for heavy lift." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed hatches in moon pool." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Load shifted X-mas tree. Land off x-mas tree on well head." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed flow line." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to ongoing operations on wellhead and hatches." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Continued to install flow line on x-mas tree." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: M/U x-mas tree clamp and pressure tested connection to 35 bar. Installed test flange on kill wing." "On 2014-04-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Ramboll done 3D surveyor for correct position of x-mas tree. Handover well to Maersk production. at 24:00 hrs." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Maersk production performing commission XMT. Installed drilling hatches for F1 and solid hatch for F6 on weather deck." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Maersk production performing commission XMT. Removed flowline F1 and connected hydraulic lines to x-mas tree. Prepared for pressure test on X-mas tree. R/U pressure test hose in moonpool. Prepared for line test." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 12.5 hours. Operational details: Maersk production performing commission XMT. Meanwhile performed pre-job meeting prior to pressure test x-mas tree. Performed line test to 380 bar. Pressure tested x-mas tree body to 35/380 bar 5/10 min. Inflow tested LMV and HMV to 300 bar for 10 min. Retrieved 6 3/8' BPV from well head. Flushed x-mas tree and closed SV. Pressure tested tubing and liner to 380 bar in steps and held pressure for 30 min. 1334 ltr pumped, 1316 ltr received. Installed flow line. Performed 3D survey of dolly tracks. Perfomed vibration tests on mud pump # 1. Preparing for R/U wire line equipment. Received well from Maersk production at 18:30 hrs." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Preparing for R/U wire line equipment." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Performed pre-job meeting and SJA prior to install wire line BOP." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.0 hours. Operational details: Positioned grease skid and bottle rack as per Aker/Schlumberger instructions. Transferred riser Joints and X/O to rig floor." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: M/U first riser joint and X/O. Land off bottom riser joint and M/U same." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Installed wire line BOP." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U wire line riser and lubricator." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.2 hours. Operational details: M/U wire line riser and L/D same on HTS. Removed 15 K line from well head area. R/U manifold and lines for wire line operations on well head area." "On 2014-04-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: P/U wire line riser from HTS and landed off and M/U to wire line BOP." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.8 hours. Operational details: M/U last 2 wire line riser joints to riser and installed lubricator. Installed elevator, t-bar, sheave and slings to TDS. Build scaffold around rotary for access." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Installed control lines from skid to lubricator." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to lift up lubricator in TDS." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Connected and lifted up lubricator in TDS. Installed quick test sub onto wire line riser." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.0 hours. Operational details: Secured control cables to wire line riser and lubricator. Transfered tools strings to drill floor." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.5 hours. Operational details: Secured control cables to wire line riser and lubricator. Transfered tools strings to drill floor." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to M/U tool string and handling guns." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.5 hours. Operational details: P/U tool string and gun assy for run # 1. Meanwhile pressure tested KWV manifold to 20/345 bar, 5/10 min." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Flushed lines and lubricator. Pressure tested lubricator and rig up to 20/250 bar 5/10 min. Meanwhile Performed pre-job meeting for handling guns." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Disconected lubricator and retracted same. M/U BHA for run # 1." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: M/U lubricator. Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Opened DHSV, HMV. and SV." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3200m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: RIH with perforation string on WL with 30 m/min according to program. Toolstring stopped moving at 3200 m / 73 deg inclination." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3600m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: RIH with perforation string on WL using tractor from 3200 m to 3600 m." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4010m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with perforation string on WL with 30 m/min to 4010 m. Correlated across good GR - DO =-2 m. Up weight @ 3860m = 5300 lbs." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3194m. The activity was categorized as 'completion -- wire line' and lasted for 1.5 hours. Operational details: Started reference pass up from 4010 m (CCL) to 3194 m @ 12 m/min." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3620m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: RIH with perforation string on WL to 3275 m. RIH tractoring down to 3620 m. Up weight @ 3590m = 5000 lbs." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4010m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: RIH with perforation string on WL from 3620 m to 4010 m." "On 2014-04-09, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3991m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Correlated tool string according to program between 3973 m to 3991 m. 2nd pass up. DO=2 m. 3rd pass up. DO=1 m. 4th pass up. DO=0.25 m. 5th pass up. Stop and add 0.5 m. DO = 0.1 m." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3991m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Correlated to position guns at interval 1 from 3973 m to 3991 m. Firing depht 3969 m." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3969m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Pressured well up to 28 bar. (Well in10 bar underbalance)" "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3969m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3973 m to 3991 m with WHP 28 bar. WHP stabilized at 33,5 bar." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 900m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: POOH from 3969 m to 900 m with perforating gun assembly no. 1." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 900m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Due to false fire alarm, lost power to Schlumberger and Aker unit. Regained power. Powered up units. Prepared for POOH with perforating gun assembly no. 1 from 900 m." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 900m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Schlumberger tested tractor prior to continued to POOH." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: POOH from 900 m to 250 m with perforating gun assembly no. 1. Powered down unit. Oceaneering recovered guide funnel and performed survey of seabed." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: POOH from 250 m with perforating gun assembly no. 1." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36 bar. Closed HMW." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and L/O guns." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Broke out lubricator at QST. L/D tractor, tool string and guns." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: P/U guns, tool string and new tractor for perforating run no. 2. Checked and tested new tractor system." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: M/U lubricator. Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Opened DHSV, HMV. and SV." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3250m. The activity was categorized as 'completion -- perforate' and lasted for 3.2 hours. Operational details: RIH with perforation string no 2 on WL with 30 m/min according to program. Toolstring stopped moving at 3250 m / 73 deg inclination." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3588m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: RIH with perforation string on WL using tractor from 3250 m to 3588 m. Correlate across pup at 3588 m" "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3933m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Correlated tool string according to program between 3936 m to 3954 m. Orientation Pass 1 -0.8 m. 2nd pass up. 3rd pass up. DO +0.2. 4th pass up. DO +0.2 m. 5th pass up." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3933m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Perforated interval from 3936 m to 3954 m Bleed down wellhead pressure from 44 bar to 30 bar prior to fire." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: POOH from 3933 m with perforating gun assembly no. 2. Shut down the unit @ 500 m." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36,5 bar. Closed HMW." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min. Meanwhile performed pre-job meeting prior to L/O guns." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Broke out lubricator at QST. L/D Gun assy no. 2." "On 2014-04-10, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Changed mystic grease on tractor." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Pumped up oil and checked tractor." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U guns, tool string and tractor." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: P/U guns, tool string and tractor for perforating run no. 3. M/U lubricator." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV. and SV." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3200m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: RIH with perforation string no 3 on WL with 30 m/min to 3200 m. Correlated across DHPG @ 2680 m." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3250m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: RIH with perforation string no 3 on WL with 30 m/min to 3250 m. Toolstring stopped moving at 3250 m / 78 deg inclination." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3588m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with perforation string no 3 on WL using tractor from 3250 m to 3588 m." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3936m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Correlated tool string according to program between 3918 m to 3936 m. Orientation Pass 1 +0.8 m. Orientation Pass 2 DO +0.2 m Orientation Pass 3. Orientation Pass 4 DO -0.4 m. Orientation Pass 5. Shooting Pass." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3915m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3918 m to 3936 m. Firing depht 3915 m. Wellhead pressure prior to fire 44 bar." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: POOH from 3915 m with perforating gun assembly no. 3. Shut down the unit @ 500 m." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36,5 bar. Closed HMW." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Inflow tested HMV with SIWHP 5 bar for 10 min. Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and L/O guns." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Broke out lubricator at QST. L/D Gun assy no. 3." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Rebuild cable head. Hot check tractor." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U gun assembly no 4." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: P/U guns, tool string and tractor for perforating run no. 4. M/U lubricator." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV. and SV." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3240m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: RIH with perforation string no 4 on WL with 30 m/min to 3240 m. Correlated across DHPG @ 2640 m. DO = +5 m. Toolstring stopped moving at 3280 m / 78 deg inclination." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3540m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with perforation string no 4 on WL using tractor from 3240 m to 3540 m. Pickup across PUP. DO=-2.2 m." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3936m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Correlated tool string according to program between 3918 m to 3936 m. Orientation Pass 1 (up to PUP for correlation proof) DO= 0m. Orientation Pass 2 DO=0.5 Orientation Pass 3 DO=0.2 Orientation Pass 4 DO =0 Orientation Pass 5 DO=0 Shooting Pass." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3885m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3888 m to 3906 m. Firing depht 3885 m. Wellhead pressure prior to fire 40 bar. WHP stabilized at 33,5 bar. Lost 200 lbs surface tension." "On 2014-04-11, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2000m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: POOH perforating gun assembly no. 4. from 3885 m to 2000 m with perforating gun assembly no. 4." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: POOH perforating gun assembly no. 4. from 2000 m. Shut down the unit @ 500 m." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 40 bar. Closed HMW." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: Inflow tested HMV against SIWHP, 35 bar for 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and L/O guns. Trouble shoot on x-tree gauge during inflow test of SV. Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Broke out lubricator at QST. L/D Gun assembly no. 4." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Checked tractor hanging. Switched to pass through mode." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to P/U gun." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: P/U gun assembly for perforating run no. 5. M/U lubricator." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV and SV." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Changed out wiper rubber on lubricator. Transfered tractor and guns for next run to rig floor. Opened DHSV, HMV. and SV." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3250m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH with perforation string no. 5 on WL with 30 m/min to 3250 m. Correlated across DHPG @ 2640 m. DO = +8 m. Toolstring stopped moving at 3250 m / 78 deg inclination." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3560m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with perforation string no 5. on WL using tractor from 3250 m to 3560 m." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2888m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Correlated tool string according to program between 3870 m to 3888 m. Orientation Pass 1. Orientation Pass 2. Orientation Pass 3. Orientation Pass 4. Orientation Pass 5. Shooting Pass." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3836m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3888 m to 3906 m. Firing depht 3836 m. Wellhead pressure prior to fire, 37 bar. WHP stabilized at 33,5 bar. Lost 300 lbs surface tension." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: POOH from 3836 m with perforating gun assembly no. 5. Shut down the unit @ 300 m." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36,5 bar. Closed HMW." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Inflow tested HMV against SIWHP, 35 bar for 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and L/O guns. Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Broke out lubricator at QST. L/D Gun assembly no. 5." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Lifted tractors to drill floor. Inspected head / hot checked for next run 6 and run 7." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: M/U tractor assembly and tool string prior to pressure test wire line BOP, riser and lubricator." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Pressure test wireline rig up to 30/250 bar, 5/10 min. Meanwhile performed pre-job meeting prior to M/U guns." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: P/U gun assembly for perforating run no. 6. M/U lubricator." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Tested QTS with test pump on rig floor to 30/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV. and SV." "On 2014-04-12, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with perforation string no. 6 on WL with 30 m/min to 300 m." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3260m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH with perforation string no 6. on WL with 30 m/min from 300 m to 3260 m. Correlated across DHPG @ 2640 m. DO = +5 m. Toolstring stopped moving at 3260 m / 78 deg inclination." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3260m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Attempted to tractor down from 3260 m. No success due to tractor failure. Troubleshoot on tractor." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 730m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: POOH with gun assembly no 6. due to tractor failure from 3260 m to 730 m. Mis-run." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: POOH perforating gun assembly no. 6 mis-run from 730 m. Shut down the unit @ 800 m." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 40 bar. Closed HMW." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Inflow tested HMV against SIWHP, 35 bar for 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and handling live guns." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Broke out lubricator at QST. Set back gun assembly no. 6. L/D tractor assembly due to tractor failure." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: P/U new tractor assembly. Installed toolhead and cable. Checked tractor and performed hot check." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U guns, tool string and tractor for perforating run no. 6. Re-run. M/U lubricator." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV and SV." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3250m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: RIH with perforation string no 6. on WL with 30 m/min to 3250 m. Re-run. Correlated across DHPG @ 2640 m. Toolstring stopped moving at 3250 m / 78 deg inclination." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3580m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with perforation string no 6. on WL using tractor from 3250 m to 3580 m." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3870m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Correlated tool string according to program between 3852 m to 3870 m. Orientation Pass 1. Orientation Pass 2. Orientation Pass 3. Orientation Pass 4. Orientation Pass 5. Shooting Pass." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3849m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3852 m to 3870 m. Firing depht 3849 m. Wellhead pressure prior to fire, 37 bar. WHP stabilized at 33,5 bar. Lost 300 lbs surface tension." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: POOH from 3849 m with perforating gun assembly no. 6. Shut down the unit @ 300 m." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36,5 bar. Closed HMW." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Inflow tested HMV against SIWHP, 35 bar for 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and L/O guns." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Broke out lubricator at QST. L/D gun assembly no. 6. L/D tractor assembly." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: P/U new tractor assembly. Checked tractor and performed opcheck, checklist, 540V hotcheck." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: M/U guns, tool string and tractor for perforating run no. 7. M/U lubricator." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV and SV." "On 2014-04-13, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with perforation string no 7. on WL with 30 m/min to 500 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3250m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: RIH with perforation string no 7. on WL with 30 m/min from 500 m to 3250 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3300m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH with perforation string no 7. on WL using tractor from 3250 m to 3280 m. Problems to get down with tractor. Worked down with tractor to 3300 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: POOH with perforation string no 7. on WL from 3300 m to 3100 m. Observed tension spike at 4600 lbs" "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3220m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: RIH with perforation string no 7. on WL from 3100 m to 3220 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3260m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Worked down with tractor to 3260 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3260m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Worked down with tractor @ 3260 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3260m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Performed meeting with town to decide on plan forward." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: POOH from 3260 m with live perforating gun assembly no. 7 due to unable to reach firing depth. Shut down the unit @ 300 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36,5 bar. Closed HMW." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Inflow tested HMV against SIWHP, 35 bar for 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and L/O guns." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Broke out lubricator at QST. L/D gun and tractor assembly no. 7. Observed 2 wheels missing on tractor." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Installed flow line on F-1. Filled flow line with MEG. Leak tested flow line to 200 bar according to procedure. Simultaneously checked backup tractors. M/U tool string with 5 1/2' drift/gauge cutter and new tractor assembly. M/U lubricator. Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV and SV." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 483m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: RIH with 5 1/2' drift/gauge and tractor assembly on WL with 30 m/min to 483 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 483m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Problems to pass DHSV @ 483 m. After 5 attempt able to pass DHSV." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2930m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: RIH with 5 1/2' drift/gauge and tractor assembly on WL with 30 m/min from 483 to 2930 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2930m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Problems to pass Mule Shoe @ 2930 m. After several attempt able to pass Mule Shoe @ 2930 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3209m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with 5 1/2' drift/gauge and tractor assembly on WL with 30 m/min from 2930 to 3209 m." "On 2014-04-14, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3280m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Started tractor and RIH with 5 1/2' drift/gauge assembly from 3209 m to 3280 m." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3685m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: RIH with 5 1/2' drift/gauge assembly using tractor from 3280 m to 3685 m." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3845m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: RIH w/ 5 1/2' drift/gauge assembly by gravity from 3685 m m to 3845 m." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: POOH with 5 1/2' drift/gauge and tractor assembly on WL from 3845 m." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36,5 bar. Closed HMW. WHP 40 bar." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Inflow tested HMV against SIWHP, 35 bar for 10 min. Meanwhile performed pre-job meeting prior to L/D 5 1/2' drift/gauge assembly." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Broke out lubricator at QST. L/D 5 1/2' drift/gauge assembly." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Checked tractor hanging. Switched to pass through mode. -540 through to line 19." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Prepared tools for rig up. P/U perforation string no 7. M/U guns, tool string and tractor for perforating run no. 7. Observed flow over top of riser." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Laid out gun assembly, connect lubricator and purged riser clean with nitrogen." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Break lubricator, and M/U guns for perforating run no. 7. M/U lubricator." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min. Filled riser with MEG. Opened DHSV, HMV and SV." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3261m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: RIH with perforation string no 7. on WL with 30 m/min to 3261 m. Re-run. Toolstring stopped moving at 3261 m / 79 deg inclination." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3610m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: RIH with perforation string no 7. on WL using tractor from 3261 m to 3610 m. Picked up across pup DO +1 m." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3814m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Correlated tool string according to program between 3817 m to 3835 m. Orientation Pass 1 up for correlation +0.8 m. Orientation Pass 2 up DO+0.8m. Orientation Pass 3. Orientation Pass 4. Orientation Pass 5. Pulled in to shoot." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3814m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 3817 m to 3835 m. Firing depht 3814 m. Wellhead pressure prior to fire, 41 bar. WHP stabilized at 41 bar. Lost 300 lbs surface tension." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: POOH from 3814 m with perforating gun assembly no. 7. Shut down the unit @ 300 m." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tools in catcher. Closed SV, 36,5 bar. Closed HMW. WHP 40 bar." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Inflow tested HMV against SIWHP, 35 bar for 10 min. Meanwhile performed pre-job meeting prior to changing out tractor and L/O guns." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bled off pressure in lubricator and purged clean with nitrogen. Pressure tested SV to 50 bar, 10 min." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Broke out lubricator at QST. L/D gun assembly no. 7. L/D tractor assembly." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Rebuild cable head. Hot checked tractor." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 4.0 hours. Operational details: Checked next tractor, opcheck, checklist, 540V hotcheck for run 8 and run 9. Prepared tools for rig up. P/U tractor and perforation string no 8. Changed wiper on lubricator." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to M/U guns, tool string and tractor for perforating run no. 8." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: M/U guns, tool string and tractor for perforating run no. 8. M/U lubricator." "On 2014-04-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Tested QTS with test pump on rig floor to 20/250 bar for 5/10 min." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Filled riser with MEG. Equalized and opened DHSV, HMV and SV." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3240m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH with perforation assy #8 on WL with 30 m/min to 3240 m. Toolstring stopped moving at 3240 m / 79 deg inclination." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3610m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: RIH with perforation assy #8 on WL using tractor from 3240 m to 3610 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3610m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Correlated across pup joint 'K' at 3588 m. DO=2,5 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3815m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH w/ run #8 by gravity from 3610 m to 3815 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3804m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Correlated across perforation interval #8 3786 - 3804 m. 1st pass up for correlation, DO=+6 m. 2nd pass up, across pup joint 'K'. 3rd pass up, DO= +1 m. 4th pass up. DO= +0,4 m. 5 th pass up, DO= +0,5 m. Oriented guns while correlating. Positioned gun with top shot at 3786 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3804m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval #8 3786 - 3804 m with WHP 41 bar. Lost 300 lbs surface tension." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: POOH with run #8 from 3804 m to 300 m. Average pulling speed 26 m/min. Shut down SLB unit." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Pulled tool string into catcher." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Closed well in as per procedure and bled down pressure. Inflow tested HMV and SV." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Broke lubricator. L/D perforation gun assy #8. All guns fired." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: M/U lubricator and performed pressure test 20/250 bar 5/10 min on W/L rig up with tractor inside (Full test required after every 5th QTS test as per AWS procedure). Bled down into closed drain. Experienced two alarms from closed drain system while bleeding down. Production dept. emptied drain tank." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Broke lubricator and L/D used tractor." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: SLB tested new tractor for perforation run #9 on deck." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: M/U BHA for run #9. Armed guns and M/U same to tool string." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator. Leak tested QTS to 20/250 bar 5/10 min. Opened well as per procedure." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3240m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: RIH w/ run #9 (perforation interval 3768 - 3786 m) w/ 4,5' OD guns by gravity from surface to 3240 m, WHP 43 bar. Average running speed 24 m/min." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3600m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with tractor activated from 3240 m to 3600 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3600m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Picked up and correlated across pup joint 'K' at 3588 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3800m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: RIH w/ run #9 by gravity from 3600 m to 3800 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3786m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Correlated across perforation interval #9 3768 - 3786 m. 1st pass up for correlation across pup joint 'K', DO=+1 m. 2nd pass up, across pup joint 'K', DO= +1 m. 3rd pass up, DO= + 0,8 m. 4th pass up. DO= +0,3 m. 5 th pass up, DO= - 0,2 m. Oriented guns while correlating. Positioned gun with top shot at 3768 m." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3786m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval #9 3768 - 3786 m with WHP 42 bar. Lost 300 lbs tension." "On 2014-04-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1900m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: POOH w/ perforation run #9 from 3786 m to 1900 m. Average pulling speed 30 m/min." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: POOH from 1900 m to 300 m. Made PA announcement and shut down SLB unit." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Pulled tools into catcher and closed in well as per procedure." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Inflow tested HMV and SV. Bled down into closed drain system. Purged riser with N2." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for L/D perforation guns." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Broke lubricator. L/D guns and tractor on deck. All guns fired." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Prepared tractor and guns for perforation run #10 (perforation interval 3640 - 3658 m)." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for M/U perforation assy." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: M/U BHA for run #10. Leak tested QTS to 20/250 bar 5/10 min. Opened well, WHP 47 bar." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3225m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: RIH w/ perforation assy #10 (interval 3640 - 3658 m), 4,5' OD guns by gravity from surface to 3225 m. Average running speed 24 m/min." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3680m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with tractor activated from 3225 m to 3680 m. Average running speed 7,5 m/min." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3658m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Correlated across perforation interval #10 3640 - 3658 m. Performed 5 passes to correlate and orient guns. Positioned guns with top shot at 3640 m." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3658m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval 3640 - 3658 m. Lost 400 lbs tension." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: POOH from 3658 m to 300 m. Shut down SLB unit." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Pulled tool string into catcher. Closed well in and bled down pressure to closed drain. WHP 49,3 bar." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Transfer pump on closed drain system tripped. Production department troubleshot and flushed system with hot water to dissolve grease. Meanwhile performed TBT for L/D perforation assy #10." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Bled down pressure in XMT cross to 5 bar. Inflow tested HMV and SV." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Broke lubricator. L/D tool string #10." "On 2014-04-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: SLB prepared and tested tractor for perforation run #11 (interval 3600 - 3609 m)." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: SLB prepared and tested toolstring #11." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for M/U perforation assy." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: M/U BHA for perforation run #11 (interval 3600 - 3609 m). Leak tested QTS to 30/250 bar 5/10 min. Filled riser with MEG and equalized pressure. Opened well. WHP: 53 bar" "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3150m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: RIH w/ perforation assy #11 (interval 3600 - 3609 m), 4,5' OD guns by gravity from surface to 3150 m. Average running speed 20 m/min." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3620m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: RIH with tractor activated from 3150 m to 3620 m. Average running speed 6 m/min." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3609m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Correlated across perforation interval #11 3600 - 3609 m. Performed 5 passes to correlate and orient guns with tractor activated. Positioned guns with top shot at 3600 m." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3609m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval #11 3600 - 3609 m. Lost 300 lbs tension." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: POOH from 3609 m to 300 m. Average pulling speed 32 m/min." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Made PA announcement and shut down SLB unit. Pulled tool string into catcher." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: Closed in well. WHP 55 bar. Bled pressure to closed drain. Inflow tested HMV and SV. Broke lubricator." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: L/D tool string on deck. All shots fired. Spooled out cable. Cut cable." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: SLB built new rope socket and prepared/checked tractor for perforation run #12." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for M/U perforation assy." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: M/U BHA for run #12 (interval 3579 - 3588 m)." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Leak tested QTS to 20/250 bar 5/10 min. Filled riser with MEG. Equalized pressure and opened well. WHP 59 bar." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3140m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH w/ perforation assy #12 (interval 3579 - 3588 m), 4,5' OD guns by gravity from surface to 3140 m. Average running speed 17,5 m/min. Powered up SLB unit at 300 m and function tested tractor." "On 2014-04-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3600m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with tractor activated from 3140 m to 3600 m. Average running speed 7,6 m/min." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3600m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Correlated across perforation interval #12 (3579 - 3588 m). Performed 5 passes to correlate and orient guns with tractor activated." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3588m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Positioned guns at shooting depth. Due to noise on CCL log, PETEC requested 2nd shooting pass. Tractored down and re-positioned guns with top shot at 3579 m - good correlation." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3588m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval #12 (3579 - 3588 m). Lost 300 lbs tension." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: POOH from 3588 m to 300 m. Average pulling speed 27,5 m/min." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Made PA announcement and shut down SLB unit. Pulled tool string into catcher." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Closed in well. WHP 63 bar. Bled pressure to closed drain. Inflow tested HMV and SV. Flushed riser w/ N2." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for L/D perforation assy." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Broke lubricator. L/D tool string on deck. All shots fired." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: M/U BHA for perforation run #13 (interval 3545 - 3554 m). Leak tested QTS to 30/250 bar 5/10 min. Filled riser with MEG and equalized pressure. Opened well. WHP 67 bar." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3150m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: RIH w/ perforation assy #13 (interval 3545 - 3554 m), 4,5' OD guns by gravity from surface to 3150 m. Average running speed 23 m/min." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3580m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with tractor activated from 3150 m to 3580 m. Average running speed 7 m/min." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3554m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: Correlated across perforation interval #13 (3545 - 3554 m). Performed 5 passes to correlate and orient guns with tractor activated. Positioned guns with top shot at 3545 m." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3554m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval #13 (3545 - 3554 m). Lost 300 lbs tension." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: POOH from 3554 m to 300 m. Average pulling speed 22 m/min." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Made PA announcement and shut down SLB unit. Pulled tool string into catcher." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Closed in well. WHP 73 bar. Bled pressure to closed drain. Inflow tested HMV and SV. Flushed riser w/ N2." "On 2014-04-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Broke lubricator. L/D tool string on deck. All shots fired." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Cut cable. Disconnected hoses and control lines from lubricator/GIH." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/D lubricator/GIH." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 3.0 hours. Operational details: L/D lubricator and grease injection head. Split same. Cleaned W/L equipment. Cleared rig floor prior to lift W/L riser." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Disconnected W/L riser from BOP. Lifted riser to rig floor applying double lift arrangement (TDS & tugger)." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.5 hours. Operational details: N/D W/L BOP and landed same on skid in moonpool. Disconnected bottom riser from XMT and lifted same to rig floor using double lift (two tugger)." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.5 hours. Operational details: Removed split hatches and installed permanent hatch on F-1 slot. R/D wireline equipment and cleared rig floor." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing Xmas tree." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Installed XMT tree cap and R/U to test XMT valves." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.8 hours. Operational details: Filled XMT with MEG using MEG injection pump. Pressure tested XMT cap to 35/345 bar for 5/15 min using AWS test pump. Bled pressure to closed drain. Pressure tested SV and KWV to 35/345 bar for 5/15 min. Bled pressure to closed drain. Meanwhile R/D and packed W/L equipment. Installed diverter." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Attempted to open HMV w/o success. Troubleshot HMV controls. Discovered local control line isolation valve on XMT accidentally in wrong position. Opened HMV." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Lined up to cement unit. Bullheaded 3 m3 MEG into well using MEG injection pump followed by 6,6 m3 packer fluid using cement pump and 1,2 m3 MEG using MEG injection pump. Closed DHSV." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Bled down pressure above DHSV to closed drain. SIWHP: 5 bar. Inflow tested DHSV for 30 min. Good test." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 3.0 hours. Operational details: Pressured up above DHSV to 75 bar. Closed HMV. Bled down pressure above HMV to 5 bar. Attempted several times to inflow test HMV, unable to obtain good test. Operated HMV, flushed tree with MEG and bled of trapped gas. Inflow tested HMV for 10 min, good test." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Inflow tested MMV for 10 min, good test." "On 2014-04-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.8 hours. Operational details: Flushed through XMT and test hoses using MEG. R/D hoses and manifold on kill wing side. Installed KWV cap, needle valve and gauge. R/U AWS test pump to P/T kill wing cap. Meanwhile lifted W/L BOP from moonpool. Disconnected AWS skid and packed W/L equipment for backload." "On 2014-04-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Pressure tested kill wing valve cap to 35/345 bar for 5/15 min using AWS pump. Good test. Meanwhile continued packing W/L equipment for backload." "On 2014-04-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Finalized and signed handover documentation. Well F-1 C handed over to production at 01:30 hrs. *** Last report on F-1 C - continue reporting on F-99 for final De-mob***" "On 2014-11-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Removed scaffolding in the moonpool. Prepared for skidding cantiliver." "On 2014-11-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.5 hours. Operational details: Skidded cantiliver from F-12 to F-1." "On 2014-11-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: Built scaffolding in the moonpool and prepared WL equipment for rigging up. Meanwhile F-1 handed over from production department to D&W." "On 2014-11-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Changed well hatch with wireline hatch. Contacted production operator and bled off XMT cross to 0 bar prior and R/U chicksan manifold on XMT." "On 2014-11-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to start rigging on well." "On 2014-11-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Removed Top cap and rigged up lower riser using tugger. Installed BOP and connected hoses. Perfomed function test of BOP." "On 2014-11-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Production operator filled lower riser section up to BOP with MEG and leak tested same. Prepared for installing upper riser section." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Lowered upper riser section and connected same. Meanwhile Altus and Halliburton tested tools on pipe deck." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Held prejob meeting. Reviewed operation and procedure for logging well." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Drilling had som issues with elevator. Fixed prior to start building lubricator." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Built lubricator on drill floor horizontally. Connected sheave wheel to spreader beam in top drive and lifted lubricator into vertical position. Meanwhile tested Halliburton tools on pipe deck." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Held toolbox talk prior to install BHA #1 into lubricator." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.4 hours. Operational details: M/U BHA #1 Tractor and PLT/RST toolstring and installed same into lubricator. Stabbed lubricator and started filling rig up with MEG used production MEG pump." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Leak tested RU to 20/345 bar 5 /10 min." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Waited on production for pumping MEG for equalizing pressure above DHSV." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Production pumped 10 m3 MEG and equalized pressure above DHSV." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Opened SV. SIWHP 62 bar." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: RIH BHA #1 Tractor and PLT/RST toolstring from surface to 500 m." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Schlumberger checked PLT/RST tools." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2925m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Continued RIH to 2925 m. Meanwhile: Held well control drill, lost air supply to grease injection skid. Held debrief. Depth P/U weight 500 m 1100 lbs 1000 m 1730 lbs 1500 m 2450 lbs 2000 m 3050 lbs 2500 m 3900 lbs" "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2925m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Correlated depth across intervall 2925 m to 2800 m." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Calibrated spinner at 10, 20 and 30 m/min in interval 2925 m to 2800 m." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3101m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Continued RIH to 3101 m, not able to get deeper by gravity." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3075m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Pulled up to 3075 m and activated tractor." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3640m. The activity was categorized as 'workover -- wire line' and lasted for 1.4 hours. Operational details: Continued RIH from 3075 m to 3640 m with tractor. Depth P/U weight 3000 m 4200 lbs 3500 m 4450 lbs Stopped at 3640 to perform correlation pass." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3523m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Pulled up from 3640 to 3523 and correlated. Observed challenge in reading CCL and porosity for correlation." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3523m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Powered down logging tools and switched to tractor. Powered up tractor." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3931m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Started tractor and RIH from 3523 to 3931 m. Observed high current draw from tractor, indicating tractor stalling out. Had normal PW at 3931 m which was HUD." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3931m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Defined 3931 as HUD. Depth was 42 m shallower than stated in program. OK to proceed." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3475m. The activity was categorized as 'workover -- wire line' and lasted for 0.9 hours. Operational details: Logged Sigma pass from 3931 m up to 3475 m at 10 m/min." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3475m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Powered down logging tools and switched to tractor. Powered up tractor." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3795m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Started tractor and RIH to 3795 m using tractor." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3795m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Switched back to Schlumberger to perform IC pass." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3660m. The activity was categorized as 'workover -- wire line' and lasted for 3.2 hours. Operational details: Started IC pass pulling 0,5 m/min from 3785 up to 3480 m according to program. Meanwhile performed well control drill: Leak below BOP." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3660m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Stopped at 3660 m. Observed cable speed ocasionally jumping between 0,2-2 m/min. Challenging to keep steady speed. Discussed with PETEC to keep speed as close as possible to 0,5 m/min. OK to proceed." "On 2014-11-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3660m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Continued to log IC pass from 3660 to 3480 m at 0,5 m/min." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3480m. The activity was categorized as 'workover -- wire line' and lasted for 3.8 hours. Operational details: Continued to log IC pass from 3650 to 3480 m. Still some challenge to keep cable speed steady at 0,5 m/min. WHP 74 bar." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3480m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Completed 1st IC pass. Powered down tool and switched to tractor." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3795m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with tractor from 3480 m - 3795 m for second IC pass." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3795m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Powered down tractor and switched line to Schlumberger. Powered up logging tools." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3795m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Started 2nd IC pass from 3785 m up to 3480 m at 0,5 m/min. WHP 80 bar." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3480m. The activity was categorized as 'workover -- wire line' and lasted for 6.8 hours. Operational details: Continued logging IC pass from 3785 m to 3480 m at 0,5 m/min. Activated tractor." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3790m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Tractored down to 3790 m at approx 11 m/min. Powered down tractor and switched to logging mode." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3790m. The activity was categorized as 'workover -- wire line' and lasted for 8.1 hours. Operational details: Logged 3rd IC pass from 3785 m up to 3474 m at 0,5 m/min." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3474m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Powered down logging tools and switched to tractor. Powered up tractor." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3931m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Started tractor and RIH from 3474 to 3931 m to perform additional PLT shut in passes. WHP 83 bar." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3931m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Powered down tractor and switched line to Schlumberger. Powered up logging tools." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3474m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Pulled up with logging tools from 3931 m to 3474 m at speed 20 m/min. Had PW at 39" "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3474m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Powered down logging tools and switched to tractor. Powered up tractor." "On 2014-11-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3600m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Started tractor and RIH from 3474 to 3931 m to perform last additional PLT shut in pass. Meanwhile discussed a tight spot observed on X/Y caliper from 3914 to 3919 m. The smalles reading was 4,2' ID on X/Y caliper." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3931m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Continued to tractor down to 3931 m. WHP 83 bar." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3931m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Powered down tractor and switched line to Schlumberger. Powered up logging tools." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Logged up from 3931 to 3478 m at speed 30 m/min. Started at 20 m/min, to avoid pulling PLT spinner to fast through restriction area at approx 3915 m." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Parked tool at 3480 m according to program. Schlumberger upladed files to interact. Production started to prepare unisolation of PWV and prepared for beaning up well." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to start beaning up the well." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Production completed unisolation plan of PWV. WHP 83 bar." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Equalized PWV using hose from KW over to production line. Opened PWV. Meanwhile Schlumberger powered up logging tools to monitor downhole." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Production beaned up well in steps obtain stable well flow. Started at 36% choke and increased in steps up to 100 %. Observed pressure dropping from 83 to 4 bar, well stopped flowing." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Attempted to flow the well. Had well on test separator against as low pressure as possible Meanwhile: Discussed further operation. WHP 6,5 bar." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 4.5 hours. Operational details: Attempted to flow the well. Had well on test separator against as low pressure as possible. WHP 6,5 bar." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 6.5 hours. Operational details: Decision made to close in well on choke to let pressure build up. WHP increased from 6,5 to 54 bar. Meanwhile discussed possiblities for further operation." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Decided to attempt to pump available nitrogen on rig, to start up well flowing the well. Production department lined up from nitrogen racks. Hooked up on wellhead on killwing manifold. Emptied 4 nitrogen racks. Was able to increse WHP from 54 -68 bar. Meanwhile Schlumberger performed stationary logging." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Equalized PWV. Production department opened choke at 100 %, took 7 min from 0 to 100 %. WHP dropped from 68 to 4 bar." "On 2014-11-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 0.9 hours. Operational details: Held choke 100 % open and observed well." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3478m. The activity was categorized as 'workover -- wire line' and lasted for 8.0 hours. Operational details: Held choke 100 % and observed well. WHP steady at 6,4 bar. Pulled up 5 meters every hour." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3459m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Discussed way forward with PETEC. Meanwhile held choke open and monitored well." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Decision made to POOH with PLT string. POOH from 3459 m to surface while logging X/Y caliper." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Closed Choke and PWV. WHP 6,4 bar. Closed SV and HMV. Pressured up XMT cross via kill wing up to 100 bar. Purged lubricator with Nitrogen." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to L/D BHA#1." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Broke lubricator and L/D BHA #1 tractor and PLT/RST toolstring." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 3.0 hours. Operational details: Pulled out cable and re-built cable head from 3/3 WP to 100% WP. Meanwhile erected scaffolding at drill floor for installing long perforation gun." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.4 hours. Operational details: Tested and calibrated tarctor and perforation tools through new cable head." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: Held toolbox talk for installing perforating guns in lubricator. Reviewed perforating procedure." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.1 hours. Operational details: Installed Tractor in lubricator. Filled 80 litres of 50/50 MEG/RX-72 in lubricator. Stabbed lubricator and tested lower QTS to 20/345 bar for 5/10 min." "On 2014-12-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.1 hours. Operational details: Disconnected upper QTS and started to install perforating guns." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.1 hours. Operational details: Continued to install perforating guns. Installed firring head and stabbed lubricator. Tested upper QTS to 20/345 bar for 5/10 min. Toolstring weight 3300 lbs in lubricator." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Opened HMV. WHP 54 bar. Equalized lubricator through kill wing manifold. Opened SV and RIH." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: RIH w/BHA #2 from surface to 500 m." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Halliburton checked connection with tool and correlated depth through DHSV." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1500m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Continued to RIH with BHA #2 tractor and perforating guns. Tried to increase speed to 35 m/min. Observed grease pump started pumping and decided to slow down speed to 30 m/min." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- perforate' and lasted for 2.1 hours. Operational details: Continued to RIH from 1500 m to 3080 m. Observed high tension on surface. Max tension observed was 9000 lbs. RIH in 100 m steps from 3000 m. Stopped at 3080 m. Pulled up and attempted to pass by gravity. NO-GO. Had to start tractor." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3200m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Started tractor and continued to RIH in 100 meters steps using tractor. Pick up weight at 3200 m was 8400 lbs." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3290m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: RIH wit tractor to 3290 m, performed pull test. PW 7500 lbs." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3590m. The activity was categorized as 'workover -- perforate' and lasted for 1.6 hours. Operational details: RIH at 100 m intervals and performed pull tests. 3490 m PW 8300 lbs 3590 m PW 9500 lbs" "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3600m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Stopped at 3600 m, had to pull over 50 % of cable strenght. Evaluated situation." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3540m. The activity was categorized as 'workover -- perforate' and lasted for 0.9 hours. Operational details: Evaluated situation, had meeting with onshore. Decided to POOH, had PW at 10 100 lbs before BHA moved, had head tension at 1350 lbs. Continued to POOH at 5 m/min, logged head tension. Depth P/U weight Head tension 3590 m 9200 lbs 2060 lbs 3550 m 8300 lbs 2009 lbs 3500 m 7700 lbs 1904 lbs 3450 m 7600 lbs 1820 lbs 3400 m 7250 lbs 1740 lbs Meanwhile evaluated situation with onshore." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.6 hours. Operational details: Continued POOH to surface." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.6 hours. Operational details: OOH, closed SV and inflow tested. Closed HMV and inflow tested. SIWHP 69 bar. Bleed down pressure in lubricator and flushed same with nitrogen." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Helt toolbox talk prior to L/D perforation guns." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.4 hours. Operational details: Waited on production department for measuring benzene." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Measured 106 ppm benzene inside lubricator. Measured no Benzene in work area for personnel." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.6 hours. Operational details: Laid down perforation guns and tractor." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 3.2 hours. Operational details: Decision made to split perforation run in two separate runs due to heavy guns. Prepared tractor and perforation guns for next run." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox talk for installing new perfoartion gun." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Installed tractor and shorter perforation gun into lubricator. Filled riser with 120 litres og 50/50 MEG/RX-72." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Checked fireing head and it was not within acceptance criteria. Changed fireing head." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.5 hours. Operational details: Connected tractor to perforation guns. Stabbed lubricator and leak tested lower QTS to 20/345 bar for 5/10 min.Opened HMV. WHP 78 bar. Equalized lubricator via kill wing. Opened SV." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: RIH with BHA #3 tractor and short perforation gun from surface to 500 meters." "On 2014-12-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Halliburton performed communication check and correlated depth in DHSV." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3097m. The activity was categorized as 'workover -- perforate' and lasted for 2.7 hours. Operational details: Continued to RIH from 500 m to 3097 meters. Toolstring stopped. Pulled up 50 meter and started tractor. Depth P/U weights 900 m 2900 lbs 1300 m 3400 lbs 1700 m 4100 lbs 2100 m 4550 lbs 2500 m 5500 lbs 2900 m 6200 lbs" "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3620m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: RIH using tractor from 3050 to 3620 m. WHP 80 bar. Stopped for correlation across pup. Pick up weight 6000 lbs at 3300 m." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3765m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Pulled up and correlated across pup joint from 3582,9 to 3588,9 m. Adjusted depth by adding 3,4 meters. Continued to RIH from 3570 m to 3765 m using tractor and perform first correlation pass across perforation depth." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3765m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Pulled up with toolstring from 3765 to 3695 m, PW 7500 lbs, observed depth was slightly off at perforation depth. Added 1,2 meters. Started tractor and RIH to 3795 m." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3795m. The activity was categorized as 'workover -- perforate' and lasted for 1.9 hours. Operational details: Continued to RIH to 3795 m to correlate depth. Pulled up from 3795 m. Observed still off by 0,6 meters on reference joint at 3730,6m. Struggled to get depth within +/- 0,5 meters due to heavy toolstring in deviated well combined with cable stretch. Performed additional correlation passes across perforation depth. Total 6 passes performed." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3741m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Performed final up pass and placed CCL at 3729,7 m with top shot at 3733 m. Lined up for fireing guns through Altus safe sub. Perforated interval 3733 - 3742,6 m. Tenson dropped 100 lbs as the guns were detonaited. Observed approx 2 bar drop on DHPG. WHP 82,7 bar. Pulled slowly out of hole after perforation." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.3 hours. Operational details: POOH with perforation string from 3660 m to surface. WHP 85 bar." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.2 hours. Operational details: Closed SV and HMV and inflow tested same. Purged lubricator with N2." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to L/D tractor and perforation guns." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Broke lubricator and laid down tractor and perforating guns." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Redressed tractor and Halliburton firing head." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: Observed one strand at the 7/16' cable almost broken. Unspooled 1450 m of cable to get cable within acceptable condition." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: Re built cable head and tested same. 100% WP." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox talk for installing BHA #4." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.9 hours. Operational details: Lifted tractor and installed same into lubricator. Installed perforation guns into lubricator. Connected firing head. Filled riser with 120 litre 50/50 MEG/RX-72. Stabbed lubricator and leak tested QTS to 20/345 bar for 5/10 min. Opened HMV. WHP 92 bar. Equalized across SV via Kill wing and opened SV." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: RIH w/BHA #4 tractor and short perforation gun from surface to 500 m. Stopped for correlating across DHSV. Meanwhile held Debrief of previous correlation pass." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Halliburton performed communication check and correlated depth across DHSV." "On 2014-12-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: Continued to RIH from 500 to 2900 m. WHP 92 bar. Depth P/U weight 500 m 2700 lbs 900 m 2950 lbs 1300 m 3400 lbs 1700 m 4050 lbs 2100 m 4650 lbs 2500 m 5450 lbs 2900 m 6600 lbs" "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3070m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Continued to 3070 m. Toolstring stopped." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3310m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Pulled up 50 meters and started tractor. RIH using tractor from 3070 to 3310 m. Tractor stalled out. P/U weight at 3300 m was 6150 lbs." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3310m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Had to pull back up and RIH again. Was able to pass on second attempt. Continued to RIH." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3620m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: RIH with tractor from 3310 to 3620 m. WHP 93,3 bar." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3570m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Correlated in short pup joint from 3582,9 to 3588,9 m. Adjusted depth by 3,4 m. Continued to RIH with tractor from 3570 to 3790 m to perform first correlation pass." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3570m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Correlated across perforation depth from 3790 to 3570 m, and verified correct depth. P/U weight was 8400 lbs when picking up from 3790 m. Observed much noise on the CCL, made it challeng to read clear CCL signals." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3700m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: RIH with tractor to perform correlation pass across perforating interval from 3790 to 3700 m. Observed the joints in the perforating area was 1 meter off. RIH again and performed a new correlation pass. The joints was within 0,5 m tolerance." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3725m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Performed final correlation. Performed final up pass and placed top shot at 3715 and bottom shot at 3724,6. Lined up for firing guns through Altus safe sub. Perforated interval 3715 - 3724,6 m. WHP 95,5 bar. Observed 250 lbs. drop in tension, and approx. 2 bar drop on DHPG. Pulled slowly out of hole after perforation." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: POOH w/BHA #4 tractor and short perforation gun from 3700m to surface." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: OOH, closed SV and HMV. Inflow tested same. Flushed RU with N2. SIWHP 96 bar." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held brief before LD BHA and perforating guns." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Lifted lubricator and LD BHA #4 tractor and short perforation gun. All shots fired." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: BHA on deck. Closed BOP and prepared for flowing well for cleanup. Observed Bird nest of cable on top of cable head (Bird nest was loose on top of cable head). Inspected cable head and counted strands of wire coming out of cable head, counted 18 pieces. Inspected along cable and counted strands, could not find out where wire broke." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: Production prepared for flowing well. Assisted production in opening HMV and equalize pressure over PWV." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Production prepared for flowing well." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Production opened up well for flowing, observed BHP dropping from 262 bar down to 250 bar as choke was opened. Got production shut down and well was closed in. Observed BHP increased from 250 bar to 271 bar." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: STBY while production department opened for production again." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: STBY while production department opened for production again. Drilling prepared AT and SJA for LD lubricator on deck and remove scaffolding on rig floor." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: STBY while production department opened for production again." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.7 hours. Operational details: STBY while production department opened for production again. Meanwhile: L/D lubricator and cut 7/16' wire, found wire strand inside tool catcher." "On 2014-12-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 3.3 hours. Operational details: Production opened up well for flowing. Observed BHP decreased from 268 bar to 259 bar. SIWHP 68 bar. FWHP dropped to 6 bar and increased and stabilized at FWHP 74 bar. Meanwhile: Pulled out and cut 7/16' cable to find broken strands. Cut 2000 meter and still not able to find area with broken strands. 4200 meter 7/16 cable left on drum." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 6.0 hours. Operational details: Flowed well to stabilize pressure and rate. FWHP approx. 75 bar. BHP approx. 258 bar. Meanwhile: Decided that 7/16' cable cannot be used in well. Prepared 5/16' cable." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 4.0 hours. Operational details: Flowed well to stabilize pressure and rate. FWHP approx. 75 bar. BHP approx. 257 bar. Meanwhile: PeTek decided not to run PLT. Started to RD WL equipment, spooled cable back to drum. RD WL winch." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 3.8 hours. Operational details: Flowed well to stabilize pressure and rate. FWHP approx. 75 bar. BHP approx. 257 bar. Meanwhile: Continued RD WL equipment." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.9 hours. Operational details: Flowed well to stabilize pressure and rate. FWHP approx. 75 bar. BHP approx. 257 bar. Meanwhile: Waited for crane." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Production closed in well. BHP 257 bar and WHP 73 bar." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.6 hours. Operational details: Closed HMV and inflow tested same. with 80 bar diff. pressure. Continued RD WL equipment." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 3.0 hours. Operational details: Opened HMV and closed DHSV. Bled pressure over DHSV to 10 bar. Inflow tested DHSV with 80 bar diff. pressure. Pressure increased 0,6 bar on 30 min." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.3 hours. Operational details: Waited for crane." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed brief prior to lift and break riser, L/D lubricator." "On 2014-12-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Lift and L/D riser and lubricator." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Spooled inn hydr hoses and BOP hoses. Tidy drill floor." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: R/D BOP, lower riser, chiksan and hoses on well head. Installed blind cap on KWV." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: Prepared pressure control equipment for backload." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.7 hours. Operational details: Filled XT-cross and leak tested top cap and KVW blind cap to 20/345 bar 5/10 min." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.5 hours. Operational details: Inflow tested SV with 130 bar diff pressure, monitored pressure on top cap." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.5 hours. Operational details: Bled of pressure in XT cross. Disconnected leak test hose from XT." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.8 hours. Operational details: Checked XT valve status. Handed well over OM. ***************** Ended operation on well *******************" "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.2 hours. Operational details: Continued preparing WL equipment for backload." "On 2014-12-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Cleaned and tidy pipe deck. Prepared remaining WL equipment for backload. Finished demobilize. ------------------------------- End of operation -----------------------------------" "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT with all involved personnel for rigging up cement spool onto XMT" "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed hatch on well F-1 C. Meanwhile: Altus prepared and lowered hoses down to moonpool for local control of HMV and DHSV." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed scaffolding around hatch. Meanwhile: Barriered off area on XT deck." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Verified no pressure on KWV prior to rigging up manifold Rigged up manifold on KWV. Installed bleed off line as per DOP." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Altus hooked up hoses for local control of HMV and DHSV. Meanwhile: Rearranged hoses in moonpool for over head crane to have clear passage." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Attempted to leak test bleed-off manifold against closed KWV with test pump, no go. Attempted to re-test, no go. Found leaking check valve on manifold. Replaced check valve and attempted to pressure test line-up to XT cross, no-go. Found newly installed check valve also leaking. Replaced check valve with lo-torque valve." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Leak tested bleed-off manifold, OK." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Opened HMV and MMV, 29bar above DHSV. Started to bleed down pressure above DHSV through KWV to closed drain." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Continued bleeding off pressure above DHSV. Bled down to 0,3bar. Closed HMV and confirmed no pressure in XT cross. Removed bleed off line and removed tree cap." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed studded tree cap connection from XT and lifted same away with tugger." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- other' and lasted for 6.5 hours. Operational details: Studded bolts found to be loose on cmt manifold and spool. Lifted cement manifold with gantry crane Rigged up high torque equipment and torqued up studs correctly, checked all other studs. Meanwhile: Installed split hatches over well F-1 C. Test ran shakers." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for installing the cement spool onto XT." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lifted cement spool and landed off on XT according to simops procedure." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U studded flange connection to XT. Meanwhile: Prepared cement hose" "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed smaller split hole cover around cement spool on hatch deck. Rigged up cement hose to cement spool. Installed safety slings." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared moonpool area." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Built scaffold in moon pool around cement spool for open and closing the lo-torq valves, and to install the drain hose on top. Meanwhile: Altus re-routed and re-installed control hoses for local control of HMV and DHSV. Hook up contingency hose from bleed-off manifold to overboard." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Continued rigging up hoses to cement spool. Meanwhile: Scaffolders continued to build scaffold in moonpool. Cementers prepared fluid for volume test of line to moonpool. Altus tested and checked hose connections for local control operation of HMV and DHSV." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Altus installed hose to closed drain on top of cement spool." "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for pressure testing the cement spool" "On 2016-06-15, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Prepared cement unit for cement operation and volume test to moonpool." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Continued preparing cement unit for cement operation and volume test to moonpool. Meanwhile: Broke off lo-torq from the cement head for volume test. Performed housekeeping in moonpool and maintenance on rig floor/derrick." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed volume test of line from cement unit to moonpool. Re-connected lo-torq to cement spool and filled cement spool with water from the cement unit. Volume from cement unit to cement spool in moonpool 900 lts." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Attempted to pressure test cement spool to 20bar/5min." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Attempted to leak test cement line to moonpool to 20bar against LTV2." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Attempted to pressure test cement unit to 20/320bar." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Halliburton investigated problem. Air in system." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Pressure tested cement unit to 20/320bar." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Performed line test from cement unit to cement spool to 20/320 bar for 5/5min. Pressure tested cement spool to 20/320 bar for 5/10min." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Opened SV Altus bled off pressure in XT cross and put 400 bar on DHSV control line." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up mud pumps to cement spool and prepared to bullhead 50/50 MEG" "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Bullheaded 3m3 50/50 MEG. Lined up and pumped 10m3 wash pill at 700lpm/75bar." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: Lined up to SW. Staged up MP#1 and bullheaded SW, 1300lpm/75bar. Pressure steadily increased to 119bar. MP1 shut down after pumping 22m3. Lined up to MP#2. Continued bullheading SW with MP#2, 1300lpm/119bar. Observed steady pressure increase to 186bar. MP2 shut down after pumping totally 55m3. Lined up to MP#3. Continued bullheading SW with MP#3, 1300lpm/186bar. Pressured increased to 239bar before starting to decrease." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Stopped bullheading after pumping 130m3 SW and monitored SIWHP, 96 bar. Staged up pump and continued bullheading SW, 1300lpm/158bar. Decreasing pressure trend." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 6.8 hours. Operational details: SIWHP after bullheading 425m3 of SW: 75bar SIWHP after bullheading 508m3 of SW: 61bar SIWHP after bullheading 586m3 of SW: 57bar SIWHP after bullheading 655m3 of SW: 55bar SIWHP after bullheading 862m3 of SW: 49bar" "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to cement job with involved personnel. Meanwhile: Continued bullheading SW, 1300lpm/122bar" "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Prepared for cement job. Meanwhile: Continued bullheading SW with rig pumps, 1300lpm/119bar." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Closed LTV6 on cement spool and opened LTV7. Released bottom dart. Mixed and pumped 20m3 1.90sg cement. Displaced surface lines with 900ltr hi-vis pill." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Closed LTV7 and opened LTV8. Released top dart. Pumped 7,1m3 hi-vis pill." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Displaced cement with 46,4m3 of SW at 1300lpm. Observed pressure increasing when cement hit top perforation. Reduced rate to 700lpm after pumping 43m3 of SW. Lined up to pump contamination pill." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pumped 3m3 contamination pill at 700lpm. Pressured built up to 67bar before dropping to 35bar. Stopped pumping and evaluated situation. Attempted to pump additional 2.5m3 of contamination pill at 700lpm. Max pressure 51 bar. Stopped pumping and discussed situation with land organization. Attempted to pump additional 1,5m3 of contamination pill at 700lpm. Max pressure 71 bar, then dropped. Stopped pumping. Appeared that suction was lost due to foam in pit and displacement tank. Total change in pit level 4,5-5m3." "On 2016-06-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lined up to mud pumps. Increased flow gently to 400lpm, pumped totally 840ltrs. Pressure built up to 101 bar rapidly. Closed in well with SV. Estimated TOC between 3080 mMD - 3110 mMD based on min/max displacement volume of 59,7/60,2 m3. Started monitoring pressure in XT cross from control room. SIWHP 27,5bar." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Monitored pressure in XT cross. SIWHP decreased slowly and stabilized at 26 bar. Cycled HMV and MMV every 1-1,5 hours. Meanwhile: Flushed kill - and cement manifold with cement unit. Attempted to pressure test cement unit." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued monitoring pressure in XT cross, SIWHP 49 bar. Bled down to 30 bar through closed drain. Continued cycling HMV and MMV every 1-1,5 hours. Meanwhile: Attempted to pressure test cement unit." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued monitoring pressure in XT cross, SIWHP 48,6 bar. Bled down to 32,6 bar through closed drain. Continued cycling HMV and MMV every 1-1,5 hours." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 6.5 hours. Operational details: Pressure tested BOP Meanwhile: Monitored pressure in XT cross. Bled off from 50 to 30,5bar. Continued to cycle HMV and MMV every 1-1,5 hours." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for inflow test and pressure test cement plug" "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 4094m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Opened SV and pressured up to 50 bar with cement unit to equalize opened HMV. Pressured up well to 310bar, 680ltr pumped from 47 bar to 310 bar. Closed SV and bled off pressure in XT cross through closed drain." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressure tested cement plug to 310bar." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Bled down pressure to 40 bar through closed drain. Continued bleeding down to 10 bar in steps of 10 bar. Monitored pressure for 10 minute at each step. Inflow tested cement plug to 38 bar differential for 30min." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Equalized pressure and opened SV. Pressured up well to 255 bar using cement unit. Closed SV Closed DHSV, bled off 340ml control fluid from control line. Bled off well to 185 bar through closed drain." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Attempted to inflow test DHSV to 70bar/30min." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Bled down pressure in well to 10 bar through closed drain Attempted to inflow tested DHSV to 245bar/30min." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: Pressured up well to 100 bar, 240lts pumped. Volume pumped iindicated that the DHSV was open. Evaluated situation." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT for inflow test of DHSV with all involved personnel" "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Prepared to inflow test DHSV. Prepared drums for volume control on cantilever. Altus prepared drain line from top of cement spool to cantilever." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pressured up well to 255bar with cement unit, 375 lts pumped from 100 to 255 bar. Totally pumped 615lts from 10 to 255 bar. No indication on test pump that DHSV opened. Bled off control line to DHSV, volume bled back 340ml." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Closed swab valve and bled off well to 234 bar, 100 lts bled back. Bled off additional 85 lts, well pressure 185 bar." "On 2016-06-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 3100m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pressured up DHSV control line to 400bar. Bled off entire well to 30 bar through closed drain. Pressured up well to 256 bar with cement unit, 604ltr pumped." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Bled off well to 185 bar and attampted to close DHSV while bleeding off pressure. Bled back 185 ltr." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Prepared space on rig floor to run WL pressure control equipment. Prepared permits, and made lifting plan for WL operations." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Inflow tested the HMV to 185 for 10 min. Bled down well from 185 Bar to 0 bar to closed drain system. Meanwhile: Prepared for wire line operations." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for rigging down cement spool" "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Drained cement spool. R/D and removed cement spool from F-1 C. Meanwhile: Built wireline riser on rigfloor." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Lowered WL adapter onto XT and installed same. Meanwhile: Continued with preparations for R/U WL equipment." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT for R/U WL equipment. Prepared permit and paper work." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed WL BOP lift cap and double securing. Transferred WL BOP from moonpool to WH. Checked O-rings on BOP and installed control hoses. Landed off lower riser and made up to XT." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: R/U hoses and manifold to WL BOP. Filled BOP with SW and performed connection test against SV to 50bar/5min to confirm O-ring seals. Removed lifting equipment in moonpool and lifted tuggers to drill floor." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed BX elevator and inserts." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U WL riser with TDS, RIH and landed off on BOP. M/U connection and L/O handling pup. Meanwhile: R/U lines from choke manifold to XT side outlets." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U QTS sub and pump-in sub. Installed 2 lo-torque valves." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U lines from choke manifold to XT outlets. Meanwhile: Prepared cable head and toolstring for cutting tubing." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed grease lines, control lines and lifted assy on lubricator. R/U sheaves to BX-elevator. Meanwhile: Mixed 50/50 MEG." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U lubricator and M/U dummmy toolstring for pressure testing. Continued to prepare toolstring for cutting tubing. Meanwhile: Flushed cement hose." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U lubricator and QTS." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Confirmed line-up and pressure tested WL rig-up to 20/345 bar for 5/10min." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT for handling explosives." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Drained lubricator to closed drain. B/O QTS. Pulled dummy toolstring out of lubricator and L/D same." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U for running WL cutter. Meanwhile: R/U chiksan and lo-torque valves from XT to choke manifold." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U for running WL cutter Meanwhile: Continued M/U chiksan and lo-torque valves from XT to choke manifold." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to arming cutter. Meanwhile: R/U hoses and chiksan in WH/XT area for circulation." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: M/U cutter to CCL and armed. Lifted tool string into lubricator, and lowered lubricator onto riser. M/U and leak tested QTS." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued M/U toolstring. Meanwhile: Continued rigging up hoses for circulation in WH area." "On 2016-06-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: RIH w/ cutter, 40 m/min. Ran slowly through DHSV from 483 mMD to 490 mMD. Unable to pass restriction at 2407 mMD." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Correlated across interval 2250 mMD and 2400 mMD . Positioned cutter at 2400 m. Activated cutter. WHP before/after cut 5 / 5 bar. DHPG read stable pressure before / after cut. No indication of cutter firing. Re-attempted to fire several times." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2410m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Checked surface equipment, OK." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: POOH with cutter toolstring into lubricator." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Closed and inflow tested SV to 345 bar/10min. B/O QTS. L/O cutter toolstring on rig floor. Insptected same. Cutter had not fired." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed TBT and handover for running new cutter" "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed muster drill. Meanwhile: Performed table top excercise on well control." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for handling explosives. Isolated TDS." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: M/U BHA for run #2. Leak tested lubricator/QTS to 20/345 bar 5/10 min." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2400m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Opened SV and RIH with cutter to 2400m. Average running speed 40 m/min. Correlated depth and cut tubing at 2400m. Positive indications of cut on XT gauge and A-annulus gauge. Lost connection with DHPG." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flowchecked well, static." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: POOH with cutter into lubricator. Meanwhile: Tested BOP" "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Closed and inflow tested SV to 345bar/10min." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for handling explosives." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: B/O QTS. L/O cutter toolstring on rig floor. Insptected same. Detonation confirmed." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for circulating via choke and poor boy gasser." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Lined up, pumped in kill wing and took returns through A-annulus outlet via poor boy degasser to slops pit. Applied 20 bar on stand pipe, opened kill wing. No pressure drop observed. Corrected and confirmed line-up." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Staged up mud pumps to 1300lpm/83bar. Circulated 1 x B/U. Stopped pumps due to H2S alarm on one portable gas detector in shaker room (3ppm). Continued circulating additional B/U at 1300lpm/83bar." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.8 hours. Operational details: Prepared and checked toolstring. M/U BHA for 7' ME plug. Leak tested lubricator/QTS to 345bar/10min. Opened HMV and MMV. Read pressure on XT cross and opened SV." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 249m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: RIH ME plug to 249m. Average running speed 40 m/min." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 249m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Correlated depth and set ME plug at 249m (mid packer element). Tagged top of plug." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: POOH into lubricator . Average pulling speed 40 m/min. Closed SV and HMV. Inflow tested SV to 185bar/10min." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to B/O QTS." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: B/O QTS. L/D and inspected toolstring." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Lined up and inflow tested ME plug to 280bar differential pressure for 10min by pressuring up through AWV. Bled off pressure to closed drain." "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to R/D wireline equipment" "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/D wireline lubricator hoses and riser. Meanwhile: Pressure tested drilling BOP" "On 2016-06-19, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D wireline BOP and lower WL riser." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Continued R/D WL BOP and lower riser. L/D lower riser in moonpool." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for removal of WL adapter and installing lifting cap" "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed wireline adapter and installed lift cap on XT. Meanwhile: Electrician and hydraulic mech. prepared to disconnect cables and hoses from XT." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Electrician and hydraulic mech. continued disconnecting electrical cables and hydraulic hoses from XT. Meanwhile: Removed wireline BOP hoses from moonpool hatch." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Prepared to remove hatches on well F-1 and F-6. Meanwhile: Continued to remove wireline BOP hoses from moonpool." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed housekeeping and PDO check in moonpool prior to lifting hatches." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed handover meeting with new drilling crew" "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U and pulled split hatch on well F-1 C." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: R/U and pulled split hatches from F-1 and pulled hatch on F-6. Removed steel beam between hatches. Meanwhile: Lifted WL BOP out of moonpool. Prepared foxhole running tool and installed same." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed handover meeting with new service crew. Prepared and activated permits. Meanwhile: Performed housekeeping and drops check in moonpool area. Pulled foxhole." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Pulled masterbushing and rotary ring. Installed hand rails. Lowered TDS lifting arrangement and installed same on XT with double securing. Lifted and held 2 ton tension. Removed XT clamp. Disconnected XT and lifted same into moonpool." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Attempted to shift load from TDS to port gantry crane. Unable to gain enough height on gantry crane to move XT into moonpool." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed new TBT to discuss situation." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Re-rigged lifting arrangement and landed XT on skid in moonpool." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Lowered 2 tuggers into moonpool and attached to XT spool. Removed NT2 connector. Disconnected and lifted XT spool through rotary and L/D same on drill floor. Meanwhile. Secured XT on skid." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed handover meeting with new drilling crew." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed outer ring and masterbushing." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Prepared multibowl for installing riser joint. Meanwhile: Removed foxhole running tool and L/O same." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Disassebled control lines from XT and installed communication collar in multibowl. Meanwhile: Cleaned and cleared drill floor." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Prepared riser joint for transfer to TDS." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for P/U and installing riser joint" "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U riser joint from HTS. Removed masterbushings and outer ring in rotary. Ran riser joint through rotary and landed on multibowl." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U NT2 connection on multibowl. Meanwhile: R/D double lifting arrangement." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installing beam and hatches on F-1 and F-6." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Installed beam and hatches on F-1 and F-6. Meanwhile: Removed WL grease skid from drill floor. Prepared slick joint and diverter for installation." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Continued installing hatches on F-1 and F-6. Meanwhile: Continued preparing slick joint and diverter." "On 2016-06-20, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Installed scaffolding in moonpool. Meanwhile: Prepared equipment for testing BOP" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Continued building scaffolding in moonpool Meanwhile: Prepared equipment for BOP test" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for removing motor from BOP crane to allow skidding BOP and for testing BOP." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed motor from BOP crane." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Tested MPR with 3 1/2' mandrel to 20/345 bar for 5/10min." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Tested kelly hose, upper and lower IBOPs to 20/345 bar for 5/10min. Meanwhile: Prepared for skidding BOP over well center." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Skidded BOP over well center and soft landed same." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for M/U NT2 connector" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Landed BOP on riser and confirmed NT2 connector landed correctly on riser. M/U NT2 connector between BOP and riser. Meanwhile: Performed TBT for testing kill manifold." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.8 hours. Operational details: Installed tension cylinders on BOP. Meanwhile: Prepared slick joint for running. Tested kill manifold to 20/345bar for 5/10min." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Installed slick joint" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Secured rotary by installing master bushings and outer ring. R/U chain sling to diverter and moved same to well center" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed master bushings and outer ring to run diverter. Ran diverter. Meanwhile: Tested standpipe manifold to 20/345 bar for 5/10min." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Aligned BOP to diverter with tension cylinders and BOP carrier. Landed diverter." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed diverter lifting arrangement. Meanwhile: M/U slick joint" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/D chain slings from TDS and installed elevator. Pressure tested diverter to 103bar and overshot packer to 20 bar." "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Filled riser with SW using rig pumps" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT prior to work on fingerboard" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for connector test" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed connector test to 20/280 bar for 5/10 min" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Adjusted fingerboad for 7in" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for rigging up handling equipment" "On 2016-06-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: R/U handling equipment for pulling tubing" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued rigging up handling equipment for pulling tubing" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT for pulling tubing" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U tubing hanger retrieval tool" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with TH retrieval tool to 20m to build landing string" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled out and installed control lines to TH retrieval tool" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with TH retrieval tool and landed out in TH at 21.1m. Locked in and confirmed 5 ton overpull" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Attempted to engage threads on TH retrieval tool to communication collar. Re-attempted several times." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Evaluated situation." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Attempted to pull tubing. Pulled with 90 ton OP, TH retrieval tool pulled free from TH. POOH with TH retrieval tool." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: L/D down tubing hanger and running tool. Inspected same, no damages." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT to move casing tong to set back area" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Moved casing tong from well center to set back area. Changed elevator inserts from 7' to 5 1/2' Meanwhile: Installed rotator. Cleaned and cleared drill floor." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Prepared to P/U spear BHA. Waited on deck crew to handle helicopter prior to pick up spear. L/O 2 ea 5 1/2' DP singles on cantilever and measured same." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: P/U and M/U spear BHA. RIH from surface to 14m. P/U 2 ea 5 1/2' DP singles from cantilever. M/U double in foxhole. M/U double to spear BHA." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2400m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: RIH with spear assy. Took up/down weight 69/66 ton. Made several attempts to pass TH at 20,7m. Rotated string w/ 5rpm/3kNm. Spear assy passed through restriction. Continued RIH to 26m. Engaged spear and P/U to 10t overpull. P/U 1,7m, 92 ton overpull (entire tubing weight)." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2398m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Indication of small pressure increase on A-annulus. Performed extended flow check on trip tank, static." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2380m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with TH and set slips" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2380m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: B/O double from TDS and released spear." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2380m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: R/U casing tong" "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2380m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: B/O and L/D 7' TH. R/B spear assy in set-back." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2380m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Dropped 2' ball and M/U 7' pump-in sub. Installed cement hose. Applied 20 bar from cement unit and verified line-up. Pressured up string and opened ME plug at 47 bar. R/D pump-in sub and cement hose." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2380m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Tested compact spider." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2367m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH from 2380m to 2367m. Removed master bushings and installed weatherford spider slips and centralizers." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2367m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Attempted to break connection. Chenged master dies on casing tong." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2367m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT prior to pull tubing. Checked all lifting equipment." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2361m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O 1 joint and 1 pup. Attached control line to spooling unit." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2183m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: POOH with 5 std 7' tubing from 2367 mMD to 2187 mMD, R/B stands. Performed LRA measurements every 3 std." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2147m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH and L/O 2 singles and joint with ME plug." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1930m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: POOH with 6 std 7' tubing from 2152 mMD to 1939 mMD, R/B stands. Performed LRA measurements every 3 std." "On 2016-06-22, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1906m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH and L/O 2 joints prior to L/D DHSV assy." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1896m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with DHSV assy and L/D same" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1579m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: POOH with 9 std 7' tubing from 1896 mMD to 1579 mMD, R/B stands. Average pulling speed 13,2 jnts/hr. Measured for LRA every 3 std. Experienced issues with casing tong unable to grip properly to break connections." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1543m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: POOH with 1 std 7' tubing from 1579 mMD to 1543 mMD, R/B stands. Worked on casing tong and changed dies." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1035m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: POOH with 14 std 7' tubing from 1543 mMD to 1035 mMD. Average pulling speed 14 jnts/hr. Measured for LRA every 3 std." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1035m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed handover meeting with ongoing crew." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1035m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed equpment check on PRS and casing tong prior to continuing pulling 7' tubing." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 881m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: POOH with 4 std 7' tubing from 1035 mMD to 881 mMD." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 881m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Isolated equipment and performed drops check on TDS and FWD PRS" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with 2 std 7' tubing from 881 mMD to 811 mMD." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Investigated damages after tugger wire caught up in FWT PRS." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Inspected and checked for loose items on top of FWD PRS" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: R/U slings and load cell to test the PRS shaft for any damage (Pull Test)" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for testing the PRS shaft" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Preformed pull test on FWD PRS R/D load cell" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT prior to moving PRS to park position" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Installed Enerpac to upper breaks to lift breaks on upper PRS trolley. Moved PRS to parked position. R/D tuggers from PRS." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Prepared tools and equipment to remove control block." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for removing control block on PRS. Meanwhile: Prepared wire for wire change on green tugger." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Removed block from FWD PRS. Meanwhile: Cleaned and cleared in locker and moonpool area." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Performed TBT with all involved personnel for PRS repair" "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: Removed control block from FWD PRS. Meanwhile: Prepared for changing wire on green tugger. Performed housekeeping in drilling areas. Performed PMs in all drilling areas." "On 2016-06-23, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed derrick inspection after work on PRS" "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Continued derrick inspection." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for continuing pulling 7' tubing" "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 751m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH with 7' tubing from 811 mMD to 739 mMD. Average pulling speed 9 jnts/hr. Needed to pull singles due to FWD PRS not operational. Lifted joints from cantilever to bay on main deck on the fly." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 751m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed dies on casing tong." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 374m. The activity was categorized as 'plug abandon -- other' and lasted for 4.2 hours. Operational details: POOH with 7' tubing from 751 mMD to 374 mMD. L/D singles. Average pulling speed 8 jnts/hr." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 302m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH with 7' tubing from 374 mMD to 302 mMD. L/D singles. Average pulling speed 6 jnts/hr." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 302m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed handover meeting between crews." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 302m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Checked equipment and changed dies on casing tong." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 243m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with 7' tubing from 302 mMD to 243 mMD. L/D singles. Average pulling speed 10 jnts/hr." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 243m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Casing tong not gripping. Changed dies on casing tong." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 212m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: POOH with 7' tubing from 243 mMD to 212 mMD. L/D singles. Average pulling speed 4 jnts/hr." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 212m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed AAR with all involved personnel for pulling tubing." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: POOH with 7' tubing from 212 mMD to surface. L/D singles. Average pulling speed 6 jnts/hr. Measured cut 4,98m below box." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Inspected and took pictures of cut. Protected cut and L/D joint." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to rigging down handling equipment." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: R/D handling equipment. Removed C/L spool and container with clamps." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared drill floor" "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT prior to P/U and RIH with combined EZSV and cutter BHA" "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U casing cutter. B/O taper mill and installed 6 5/8' to NC50 and NC50 to 5 1/2' FH XO." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U EZSV RT and M/U to cutter. Installed EZSV plug on RT." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Measured distance from bottom EZSV to casing cutter." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U single and RIH from 13,5 mMD to 21 mMD." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Installed power rollers behind HTS on cantilever." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Performed TBT prior to P/U 5 1/2' DP singles and RIH. Checked all equipment and barriers." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Troubleshot issues with rotator on elevator." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed TBT prior to P/U 5 1/2' DP in singles." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 93m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U singles while RIH w/ EZSV/Cutter BHA on 5 1/2' DP from 21 mMD to 93 mMD." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 93m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed master bushings and installed auto slips." "On 2016-06-24, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 375m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: P/U singles while RIH w/ EZSV/Cutter BHA on 5 1/2' DP from 93 mMD to 375 mMD. Average running speed 141 m/hr." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1198m. The activity was categorized as 'plug abandon -- cut' and lasted for 3.2 hours. Operational details: P/U singles while RIH w/ EZSV/Cutter BHA on 5 1/2' DP from 375 mMD to 1198 mMD. Average running speed 253 m/hr." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1198m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: M/U TDS and filled pipe w/ 400 l/min. Pumped 615 strokes/13,6 m3." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1313m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: P/U singles while RIH w/ EZSV/Cutter BHA on 5 1/2' DP from 1198 mMD to 1313 mMD. Average running speed 153 m/hr. Experienced issues with HTS." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1313m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Troubleshot issues on HTS. HTS not feeding pipe all the way to elevator." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1393m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U singles while RIH w/ EZSV/Cutter BHA on 5 1/2' DP from 1313 mMD to 1393 mMD. Average running speed 160 m/hr. Unable to get proper latch on elevator." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1393m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed elevator." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1503m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U singles while RIH w/ EZSV/Cutter BHA on 5 1/2' DP from 1313 mMD to 1409 mMD." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1503m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed power rollers and set up to run stands from derrick." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1744m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ EZSV/Cutter BHA on 5 1/2' DP from 1503 mMD to 1744 mMD." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1812m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Continued RIH EZSV/Cutter BHA on 5 1/2' DP from 1744 mMD to 1812 mMD, restricted speed due to packer" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1812m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: TBT and equipment checks" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2179m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Continued RIH with EZSV and casing cutters from 1812m to 2179m restricted due to packer" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2179m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Investigated fault on draw works motor 3" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2348m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Continued RIH from 2179m to 2348m restricted due to packer" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U wild single from cant. for space out and RIH from 22348m to 2362m" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Filled pipe 400 lts/min. Up wt 147, Dwn wt 132" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2390m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Set EZSV plug at 2390m mid element. 38 turns and pull up in 9T increments. Pins sheared at 169T. Pulled up 2m and rotated string 25 turns and tag with 7T" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2390m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Spaced out and lined up for pressure test of EZSV. Close UPR. Verify line with 20 Bar. Pressure tested 20 bar, 5 mins/ 165 bar, 10 mins. Lined back up for drilling and opened BOP" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Pulled up to cutting depth, took up wt 146T and down wt 131T Rotating torque with pumps off at 100 rpm 5-10 Knm rotating wt 138T, Mud pump pressures at 300lts/ min 12 Bar, 400lts/min 34, 500lts/ 53 Bar." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: TBT for cutting the 9 5/8in casing" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Started cutting 9 5/8in casing, staging up mud pumps 300lts/ min 16-17 Bar then up to 400lts/ min 33 Bar 80 RPM, Tq 8 Knm. Cut at 2374m. Pressure dropped from 33 bar to 0 bar. Torque went down to free rotation value." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flow check well on trip tank. Static" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Started mud pumps 400lts/ min 0 Bar. Picked up 0.5m and observed stand pipe pressure increased to 33 Bar, carefully RIH and observed pressure drop at 2374m to 0.8 Bar. Set 2T on blades to verify cut. Measured cut window 10 cm. ." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: H2S detected on the Baker gas trap in flow line. Discuss and plan next phase in operation" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: Circulated 2 x bottoms up staging up mud pumps to 1700 lts/ min 30 Bar. No gas detected in shakers. Baker gas trap showing 2 ppm H2S in fluid." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2374m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Lineed up over trip tanks and installed mud bucket line" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1543m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: POOH wet with mudbucket from 2389m to 1543m" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1543m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: TBT with new crew" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 752m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: POOH from 1543m to 752m." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 752m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Layed out wild sgl to cat walk." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 334m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: POOH from 738m to 334m." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 334m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Changed out auto slips." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 13m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: POOH from 334m to 13m." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Broke down BHA, inspected same" "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor after trip." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: TBT for running MST ret tool." "On 2016-06-25, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pick up MST ret tool and function same prior to running" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Run and landed out on MST ring, engaged as per GE instructions" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Made up TDS, 75t overpull to pull mst seal." "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with ret tool" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed control lines, rigged down spooler, layed out retrieval tool." "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Serviced drilling equipment" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting/Brief/Debrief" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Picked up cutter BHA and inspect same" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Picked up sgl and RIH with cutter from 13m to 130m." "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Made up TDS and filled string" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 130m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Took parameters at 330 lpm, 29 bar, 400 lpm, 51 bar, up wt 74t, dw wt 71t,, free rot tq 5 knm, Cut csg as per well bore instructions at 130m" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Pumped out of hole from 130m to 15m due to not enough weight below spear" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Engaged fish with the spear, POOH, csg hanger on surface, inspected same" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: TBT for rigging up csg handling equipment" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.8 hours. Operational details: R/U handling equipment" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: TBT prior to pulling 10 3/4 tie back" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Attempted to break first connection. No go. Torque too high to break. Remove slip guides for adjustable sub Assy to pass and pull up to next connection" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: POOH with 10 3/4 tie back to surface. Length of off cut 6.85m" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: TBT for rigging down casing equipment" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: R/D casing equipment. Install BX4 elevators" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: TBT for running in hole with GE jetting sub and torque tool" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Picked up jetting sub with torque tool and XO 6 5/8 to 5 ½ FH Made up and run in hole laying out first single 5 ½ DP for space out. Checking torque on all connections" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Washed down from 134m 1500lts / min 23 bar increasing to 33 bar stopped pumps and tag tie back Assy @140m" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Released tie back w/ 3 turns. Tie back broke at 25 KNM" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH and pick up single 5 ½ DP back into string and lay out BHA to canteliver" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Picked up spear Assy from Canteliver and RIH from surface to 143m (land off point)" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 144m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Tagged @ 143.48m bit depth with 3T, picked string up to neutral weight and turn string 4 turns LH to unscrew remaining threads on adaptor. Started mud pumps and pressured up to maintain minimum 15 bar. 1050lts/ min 16 Bar, picked up string to 140m and increased pump rate to maintain minimum 15 Bar pressure in string, 1170lts/ min 16 Bar, picked up to 139m and increase pump rate to maintain minimum 15Bar pressure 1500lts/ min 20Bar" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Engaged spear and POOH. Fish not on spear" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: GE and wellbore inspected tools. Wellbore tool found to be in release position due to LH turns in string to release well head adapter. Reset tool" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 144m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: RIH with spear assy. And engaged spear, 4T overpull observed" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: POOH with spear assy. Fish not on spear." "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Inspected tool and reset. L/O spear assy" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: P/U assy with different type of spear (Itco spear w/ grapple), inspected and doped" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Drill. Table top talked GAS procedure and experience transfer." "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: TBT prior to running spear" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.2 hours. Operational details: RIH from RKB to 130m, Engaged fish and pulled free with 30t overpull. Pulled to surface, secured and disengaged fish" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Layed out fish to deck, inspect and layed out spear" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor of excess equipment" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: TBT for picking up and running guns" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.8 hours. Operational details: M/U gun BHA, changed dies in iron roughneck for some of connections" "On 2016-06-26, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: RIH from RKB t0 130m, closed BOP and circulated with 200 lpm, 2 bar. to confirm line up" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Broke connection, dropped ball, RIH to firing depth. Perforated interval 141m - 147,4m" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Closed BOP, lined via fully open choke, pressured up string to 135 bar, observed shear" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Circulated via poor boy to check for gas with 250 lpm, 1 bar. Pumped 2.3m3 to get stable returns" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Flow check via choke" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Opened BOP, lined up and flow checked on trip tank, well static" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: POOH from 148 m to 16m" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Inspected and layed down BHA. All shots fired" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Change handling gear back to 5.5 elevators and iron roughneck" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: R/D perforation handling equipment and cleared rig floor." "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Pickup milling BHA from cantilever, RIH from surface to 5m" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for handling milling BHA and rig tongs" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: R/U tongs and M/U magnet to 68knm" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: R/D rig tongs" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: Continued P/U milling BHA" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: M/U TDS and fill pipe" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Recorded parameters 2000lts/ min 5-7 bar. Up wt. 78T, down wt. 74T without rotation, free rotation torque with 80 rpm, 0-3 KNM, rotating weight 76T. Run in and tagged at 140.86m bit depth" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 8.0 hours. Operational details: Pulled up 1.5m, established parameters and commenced milling. 2000lts/ min 5-7 Bar, 80 RPM, 2-4 KNM, WOB 1.3T. Milled from 141.26m to 141.46m. Picked off bttm and spaced out due to leaking fittings on BOP" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Repaired leaking fitting on BOP" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Lineed up and started milling from 141.06m to 141.07m, 2000 lpm, 5 bar, 120 rpm, 5-15 knm" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.5 hours. Operational details: Continued milling @100-120RPM, 1-3t WOB, 2000lpm, 3-11KNM, 5-7bar. Stopped due to no progress" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Attempted to R/B DP stand, no success. Observed connection above saver sub broke when trying to break out stand from TDS" "On 2016-06-27, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: R/B stand of DP with saver sub. Broke connection with 150KNM" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: R/B stand of DP. Broke connection w/ 150KNM. Inspect TDS after milling operation. Broke saversub w/ 100KNM" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: M/U saversub to TDS. R/B stand of DP" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: POOH w/ milling BHA to surface, inspect same, cleaned magnets, 6 kg metal recovered from magnet (very fine swarf). Some wear observed on the cutting faces of mill" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: M/U BHA w/ new milling assembly" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: M/U 2ea stands of DP, M/U TDS, established circulation" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 7.8 hours. Operational details: Milling out 10 3/4in casing hanger. @ 100-120 RPM 1-3 WOB, 2000 LPM, 3-11 Knm, 5-7 BAR String stalled out several times @ 24Knm. +/-25 overpull to free pipe. Milled from 140.98m to 141.10m. Very slow progress" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.8 hours. Operational details: Continued milling out 10 3/4in casing hanger. @ 100-120 RPM 1-3 WOB, 2000 LPM, 3-11 Knm, 5-7 BAR String stalled out several times @ 24Knm. +/-25 overpull to free pipe. Milled from 141.10m to 141.23m. Improved progress. Got traces of H2S of 12 ppm" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: Picked of bttm and circulated clean while discussing way forward. Data indicated that mill has passed the hanger, estimated 20cm below planned milling depth, it was decided to POOH w/ milling BHA and attempt to pull csg" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Unable to break out connection. Broke out double and layed out same." "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 141m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: DROP check on TDS" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 85m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: POOH from 110m to 12 m, all connections over torqued" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Pulled mill and magnet assy, 1,5kg fine swarf recovered from magnets. Cleaned magnets, checked mill in gauge, observed normal wear on cutting faces" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Layed out mill assy to deck" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to P/U BHA" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: M/U spear BHA #19" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH spear BHA on DP to 135m spear depth. L/D single for spaceout" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: M/U TDS to string. Recorded weights. Weight Up 76T, Weight Down 74T, Free rotation 75T, 3RPM, 0,5KNM" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH while pumping @ 300LPM. Tagged hanger w/ 12,25 guide sleeve @ 140m, spear depth @ 153,4m. Attempted to engage spear. No success." "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH w/ spear BHA #19, inspected spear, ok. Set spear in catch mode." "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH w/ spear BHA #20 until 12,25 guide sleeve is just above hanger @ 140m" "On 2016-06-28, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Attempted to engage spear to fish. No success. Tagged hanger with 12,25 guide sleeve and set down 5T" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 153m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled up and observed 10T overpull" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH spear BHA #20 and inspected same, spear ok" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 65m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Broke off 12,25 guide sleeve. P/U single DC" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH spear BHA #21 to 155m. L/D single for space out. M/U TDS to string" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 156m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Engaged spear to fish @155m. Pulled 8T overpull. Slacked off weight. Spear released. RIH spear to 156m. Engaged spear and pulled to 270T (40t overpull). Fish is not free. Moved string up/down between 150T-270T several times. Fish not free. Pulled in steps to max 320T on Martin Decker (90t overpull). Measured stretch in pipe - 3,2m. Estimated neutral point depth @ 2300m" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Released spear. POOH to surface. R/B spear in derrick. Observed damage on grapple (crack)" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Cleaned drill floor" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U cutter BHA #22" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 169m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: RIH w/ cutter BHA #22 to 169 m" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 169m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Installed auto slips" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 692m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH from 169 m to 692 m. Filled string" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 692m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: Waited on further instructions, Meanwhile carried ou rig floor maintenance and PM" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1600m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: RIH from 692m to 1600m" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1600m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Filled string" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2340m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: RIH from 1600m to 2340m. Picked up 2 singles from deck for space out" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2363m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Took cutting parameters and cut csg at 2361m with 330 lpm, 100 rpm, 9-11 Knm" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 5.2 hours. Operational details: Observed overpull when picking up work string between 138t and 300t on martin decker. String stuck @ 2362m. Tried to work string free. Max pulled to 320t, max torque 40knm, sat down all string weight. No success to get string free. Evaluated further steps, started mobilizing WL cutter equipment to cut inside DP." "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Waited on further instructions, meanwhile drillfloor prepared to work on PRS" "On 2016-06-29, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Waited for WL cutting equipment and personnel to be mobilized. Meanwhile worked on repairing forward PRS" "On 2016-06-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 10.0 hours. Operational details: Waited for WL cutting equipment and personnel to be mobilized. Meanwhile worked on repairing forward PRS. Greased manifolds" "On 2016-06-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Waited for WL cutting equipment and personnel to be mobilized. Meanwhile test run forward PRS" "On 2016-06-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Waited for WL cutting equipment to be mobilized. Meanwhile worked on repairing forward PRS. L/O stand of 7in tbg" "On 2016-06-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Waited for WL cutting equipment to be mobilized. Meanwhile worked on repairing forward PRS, trouble shoot PRS setdown load indication. Prepared for WL work. Changed out PS21 to master bushings, cleared rig floor." "On 2016-06-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Waited for WL cutting equipment to be mobilized. Meanwhile L/O 7in tbg stand from derrick. Rig down csg tong equipment, prepared to break out and changed spear assembly" "On 2016-06-30, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Worked on preparing WL cutting equipment, hooked up logging container. Meanwhile prepared flat bottom milling assembly for the dress off run. Changed out damaged grapple on spear stand. R/B same" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- repair' and lasted for 7.0 hours. Operational details: Worked on preparing WL cutting equipment: built up WL tool string on pipe deck, prepared winch. Meanwhile picked up 10 3/4 cutter assy and broke off cutter, redressed knives on cutter for 9 5/8 casing. L/D same" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: TBT before installing sheeves and picking up wireline string" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: M/U tool string" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2362m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Checked WL cutter tool string and positioned top sheave over drill string" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: RIH w/ WL cutter from surface to cutting depth of 2346m. Correlated by CCL log" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2346m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Applied 10 Ton overpull to drill string, 153T on Martin Decker. Set WL anchor. Cut csg. Took 7 min to make cut" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2346m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Observed back flow from drill string" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2346m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Released WL anchor. Set tool for POOH" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: POOH w/ WL cutter from 2346 m to surface" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: L/D WL tool string" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Circulated BU @ 900 lpm, 7.5 bar, 1.1sg fluid in returns. Meanwhile R/D WL equipment. Changed master bushing to PS 21" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Flow checked well. Static" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2320m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: POOH w/ drill pipe from 2346m to 2320m L/D out 2 x singles" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 868m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.5 hours. Operational details: POOH w/ drill pipe from 2320m to 868m" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 868m. The activity was categorized as 'interruption -- repair' and lasted for 4.2 hours. Operational details: Repaired leak on aft PRS. Changed out burst hose on main arm" "On 2016-07-01, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH 5 ½ DP to surface" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Changed PS21 slips to master bushing, L/D last stand w/ cut DP single" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting before P/U flat bottom milling BHA" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 35m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: P/U and M/U flat bottom milling BHA" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: RIH w/ flat bottom milling BHA to 135m, P/U and M/U space out pup" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: M/U TDS to string. Recorded parameters: 2000 lpm - 6 bar, 77t up weight, 74t down weight, 76t at rotation 80rpm, 2-4kNm. RIH slowly and tagged hanger @140m" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Reamed hanger area @ 140 -140,5m. 120rpm - max 15kNm, 2000lpm, 1-2t WOB. Stopped rotation and passed hanger area 2 times. No overpulled/set down weight observed" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 153m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: RIH slowly and tagged top of fish @ 153,1m" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 153m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Dressed off top of fished. Milled 10 cm. 120 rpm - 7-10kNM, 2000 lpm - 6bar, 1-3t WOB" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 150m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Pulled 3m from top of fish and circulted @ 3500lpm 2 B/U, 20bar" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 31m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: POOH from 150m to 31m, L/D DP Pup used for spacing out" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: L/D flat bottom mill BHA. Clean magnets and gauged/inspected mill. Full gauge on mill. 11.5kg of metal swarf removed from magnet" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting before M/ spear BHA" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 22m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: M/U spear BHA w/ guide sub" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 153m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH with spear BHA from 22m to 153m" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 153m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Engaged spear. Pulled fish free with 50t overpull, 290t on weight indicator" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH on DP with spear and fish on surface" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: P/U and MU 6m pup joint for handling spear BHA, secured fish at rotary, released spear from fish" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Cleaned and serviced spear grapple, R/B spear BHA, Cleared and cleaned rig floor" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for R/U csg pulling equipment" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2361m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/U handling equipment for X casing" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2341m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: L/D first joint with pup joint of 10 3/4 csg" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2341m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Changed out master bushing to PS 21" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1741m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 4.5 hours. Operational details: POOH w/ 10 3/4 csg from 2341 to 1741. Pulling @ average 8,6 joints/h, maximum @ 12 joints/h. Difficult to break some of the connections. Need to hit with sledge hammer" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1741m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.2 hours. Operational details: Changed csg handling equipment to pull 9 5/8csg" "On 2016-07-02, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1290m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 3.5 hours. Operational details: POOH w/ 9 5/8 csg to 1290 m. Pulling @ average 11,4 joints/h, maximum @ 12 joints/h" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 7.5 hours. Operational details: POOH w/ 9 5/8 csg from 1290 m to 3 0m. Pulling @ average 12,7 joints/h, maximum @ 15 joints/h" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed weekly fire drill. Kick drill 42 sec to secure the well." "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Pulled from 30m to surface the remaining joints. No fish observed on the last joint" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for rigging down csg pulling equipment" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.0 hours. Operational details: R/D csg pulling equipment" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Cleaned rig floor" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting before P/U 13 3/8 EZSV plug" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: P/U and M/U the EZSV running tool, installed EZSV plug and loaded centralizer springs" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed master bushing to PS21" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2338m. The activity was categorized as 'plug abandon -- other' and lasted for 5.0 hours. Operational details: RIH w/ EZSV BHA from surface to 2338 @ 2min/std" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2338m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Took parameters: PU weight 144t,SO weight 130t. Broke circulation @800lpm, 9,2 bar. Washed setting area between 2337m to 2343m" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2340m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Set EZSV plug @ 2340m. 10rpm, 37 CW turns, P/U to 154t, held. P/U to 164t, held. Pin sheared@ 28t overpull" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2340m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: P/U to 2337m, circulated @ 2600lpm, 38bar. Increased in steps to 3500lpm, 60bar. H2S on shaker 103ppm in mud and 2ppm in air. Meanwhile M/U pump-in sub assembly for cement job" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2337m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Continued to circulate 2 BU @ 3500lpm, 65bar, 30rpm, 2-5kNm. Circulated until H2S level is down to 0. Meanwhile performed TBT for cementing operation and pressure tested cement line to 100bar" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2337m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: R/B stand, P/U pumping sub assembly, M/U TDS" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2337m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed cementing hose, lined up cementing line. Pressure tested connection between pumping sub and LTV. Observed leak on LTV." "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2337m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed out LTV, re-tested cementing line up to 100bar. Good test" "On 2016-07-03, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2337m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Placed balanced cement plug (2340 m - 2137 m ): Pumped 20 m3 of wash pill spacer, 2500 l/min/ 33 bar. Mixed and pumped 19,3 m3 of 1,9 SG cement slurry, 600-800 l/min. Displaced the cement to the rig floor with 1000 l of drill water. Zeroed volume counters. Displaced the cement with 22 m3 of sea water, 2700 l/min. Broke and L/D pump in sub assembly." "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2137m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ 5 stands to 2137m" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2137m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Circulated out excess cement @3500lpm. After 132m3 pumped diverted returns to wash pill slop pit. Could not clearly identify cement in the returns. After 90m3 pumped diverted flow into active pit. Totally circulated 288m3" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.5 hours. Operational details: POOH w/ DP and EZSV setting tool" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.2 hours. Operational details: WOC, meanwhile worked on Wellbore assemblies, prepared for the next run. Performed rig floor inspection and maintenance" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 81m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: P/U and M/U tagging BHA and RIH from surface to 81m" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 81m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Changed out master bushing to PS21" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: RIH w/ tagging BHA from 81 to 140m. Met restriction @ 140m, hanger area" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.5 hours. Operational details: M/U TDS, milled hanger area: 100-140 RPM/1500 lpm/1 bar/1-2t WOB. Pipe stalled several times @20kNm. Pulled up to 15t to free pipe. Removed PS21 due to vibration of the pipe" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Performed drops inspection on TDS. Installed PS21" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1375m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: RIH on drill pipe from 140m to 1375m" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1375m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Encountered restriction @1375m Pulled 40t overpull to free pipe. M/U TDS, established parameters: 1500 lpm/4 bar/80 rpm/3-6kNm" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1377m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Milled through restriction from 1375 to 1377m 2000 lpm/12 bar/120 rpm" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2099m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.5 hours. Operational details: RIH on drill pipe from 1377 m to 2099 m. Encountered top of cement @2099 m" "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 2100m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Dressed off 0,7 - 1 m: 120 rpm/ 2000 lpm/6-12kNm. Tagged top of cement w/ 10 t @ 2100 m." "On 2016-07-04, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1830m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ tagging BHA from 2100 m to 1830 m" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1693m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH from 1830m to 1693m" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 1693m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Worked on load handling and slew fault on aft PRS. Reset" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 95m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.2 hours. Operational details: POOH with tagging BHA from 1693m to 95m" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 95m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Meanwhile removed PS21 and installed master bushing" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: L/D HWDP and tagging BHA" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: M/U 13 3/8 csg cutting BHA" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: RIH w/ 13 3/8 csg cutting BHA to 850m" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: M/U TDS, filled string, recorded parameters: 97t weight up, 93t weight down, 95t free rotation w/ no flow, 100 RPM, 2-6 Knm. w/ 300 lpm 18Bar, 500lpm 56Bar, 600 lpm 76Bar" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cut 13 5/8 casing @ 850m. 80rpm - 9kNm, 500lpm - 56Bar. Good indications of cut, heard sound on surface" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min - Static" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 9m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: POOH from 850m to 9m. Pulled wet, used mud bucket" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting before L/D csg cutter BHA" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Changed PS21 to master bushing, L/D cutter BHA. Inspected knives, in good condition" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor. Meanwhile changed dies on aft IR and aft PRS" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 43m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: P/U 13 3/8 EZSV and M/U same to running tool. Installed centralizer springs on running tool and M/U to stand of 5½ drill pipe" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 43m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21 slips" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 842m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: RIH w/ EZSV plug from 43m to 842m 2min/stand" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 842m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS, circulated at 800lpm for 3min. Moved pipe up and down from 842mto 838m while circulating" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Set 13 3/8 EZSV plug at 840m, sheared out of plug with 27 ton over pull and set down 6 ton to check EZSV set. Pulled up 3m and rotated 27 turns to the right to release tool" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Circulated bottoms up 3 times. H2S gas readings on Baker sensors in gas trap is max at 9ppm. Parameters: 2500 lpm at 21 bar, 50 rpm , 1-3 kNm. Observed OBM in returns. Stopped circulating with 0ppm H2S" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 807m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/B one stand and dropped 3 inch drift" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH from 807 m to surface" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed PS21 to master bushing" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: L/D EZSV running tool. Pressure tested 13 3/8in EZSV to 40 bar from above. Good test. 520 ltr pumped and 520 ltr returned" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U guns" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: M/U TCP guns BHA" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 151m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: RIH w/ gun BHA at 1 min/stand. Filled pipe, confirmed line up. Took up/down weights: 73t/70t" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 151m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.7 hours. Operational details: Disconnected TDS, dropped 1,375in ball into the string, M/U TDS to the string. Closed UPR, pressured up string to fire guns. Guns fired at 120bar. Good indication of firing guns: 'bang' sound and light string movement. Top shot at 141,5m, bottom shot at 151,2m" "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 151m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Staged up pumps to 1350 lpm, circulated for 10 min, took returns through the choke. Max H2S in returns 13 ppm on Baker sensors in gas trap. Flow checked well on choke, stable. Opened upper pipe ram. Flow checked well for 10 min. Stable." "On 2016-07-05, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: POOH w/ perforation BHA, 3x stands and 1x single" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: C/O elevator inserts to 4.5in inserts. L/D perforation guns BHA, inspected BHA, all shots fired. C/O elevator inserts back to 5.5in inserts" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U EZSV setting tool" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 820m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: RIH w/ EZSV setting tool to 163m, installed PS21, continued RIH to 820m" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Broke and M/U 1x double and 2x 3m pups for spaceout pump-in sub. M/U pump-in sub, cementing hose w/ LTVs. Recorded up/down weights 97t/91t. RIH and stang into EZSV w/ running tool w/ 10t set down weight." "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for displacement annulus behind 13 3/8in csg," "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: Circulated annulus behind 13 3/8in csg to clean sea water, increased flow rate from 250 to 1250lpm, pumped 2 BU or total of 144 m3, until clear sea water confirmed in returns. Observed H2S of max 14ppm on Baker sensor in gas trap. No H2S in air measured on gas sensor in shaker room. Treated returns with SOURSCAV to remove H2S and Soda Ash (to increase pH) to prevent forming new H2S" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Flow checked well on full opened choke: Static. Opened UPR and continued monitoring well on trip tank. Static. Meanwhile performed TBT for cement job" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Performed line test prior to cement job to 100 Bar. Good test. Checked line up, Prepared for pumping cement job" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Cement plug in annulus between 13 3/8in csg and 20in csg. Theoretical height from 850m to 450m (TOC). Pumped 20 m3 of wash pill, 1200 l/min/ 13 bar. Mixed and pumped 35 m3 of 1,9 SG cement slurry, 600 l/min. Displaced the cement with cement unit with 11 m3 of drill water, 1200 l/min, pumping pressure went up to 50 bar." "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 840m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Stang out of EZSV w/ running tool, P/U 3.5m above EZSV. Balanced cement plug. Theoretical height from 840m to 740m (TOC). Mixed and pumped 7,7 m3 of 1,9 SG cement slurry, 600 l/min. Displaced the cement with cement unit with 7,8 m3 of drill water, 800 l/min, pumping pressure of 10 bar." "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 730m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Broke off cement hose and checked for backflow: no backflow observed, string on vacuum. L/D cement assembly. POOH from 836.5m to 730m 2 min /stand" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 730m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: P/U single with 2 x sponge balls installed and M/U TDS. Circulated at 2500 l/min, 19 bar, 50 RPM, 2-4kNM until clean returns confirmed. Totally pumped 3x bottoms up (120m3). Meanwhile flushed manifolds after cement job" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: POOH from 730m to 85m. Removed PS21 slips and installed master busing. Continued POOH to surface. L/D EZSV running tool" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Cleaned rig floor after cement job, broke out cement assembly and L/D same" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.0 hours. Operational details: M/U BOP jetting sub and washed/jet BOP with 1500 LPM at 3 bar. Broke off jetting sub and R/B stand" "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.0 hours. Operational details: WOC. Meanwhile carried out maintenance on AFT and FWD PRS, DW, TDS, AFT IR." "On 2016-07-06, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 5.0 hours. Operational details: WOC. Meanwhile worked to install csg tongs on fox hole side. Continued maintenance TDS, housekeeping in shakers, prepared tools and equipment for N/D diverter and BOP. Refilled gearbox oil on TDS" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: WOC. Meanwhile removed tools and equipment from TDS, prepared tools and equipment for N/D diverter and BOP. Moved fishing equipment from cantilever to free up space for 7in tbg. Moved new lifting cap for cementing spool into moonpool." "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: WOC. Meanwhile worked to L/O 7in tubing from derrick. Issues with coupling hanging up on upper claw when repositioning PRS at foxhole. Continued to prepare tools and equipment. Continued hosekeeping in shakers." "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: WOC. Meanwhile worked to L/O 7in tubing from derrick. Difficulties to breakout connection w/ csg tong. Continued to prepare tools and equipment. Continued hosekeeping in shakers" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: WOC. Meanwhile worked to L/O 7in tubing from derrick. Layed out 1x stand." "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: WOC. Meanwhile worked to install bolt on TDS blower cabinet" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: WOC. Meanwhile worked to L/O 7in tubing from derrick. Layed out 2x stands." "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pressure tested surface cement plug against closed shear ram. Attempted to test twice. Pressure broke off around 30-40bar and leaked off. After second attempt started loosing fluid into the well around 1,6m3/hour" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 11.0 hours. Operational details: Continued to layout 7in pipe from derrick. Layed out 9x stands. Meanwhile continued w/ maintenance work on TDS and DW. Function tested BOP. Continued preparation to N/D BOP. Losses 1,6m3/hour. Meamwhile evaluated with onshore organization further plans" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to run RTTS plug" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.8 hours. Operational details: RIH 3x stands 8,25in DC and RTTS BHA. Losses 1,6m3/hour" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH on 5,5in DP to 130 w/ RTTS plug BHA. M/U pup joint for space out and connected TDS. Placed RTTS packer at 131,5m (middle element). Filled pipe and broke circulation. Recorded up/down weights 88t/84t. Losses 1,6m3/hour" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Set RTTS Plug at 131,5m (middle element). Closed UPR on BOP and lined up cement unit for pressure test below RTTS via drill string. Losses stopped after RTTS packer was set" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Pressure tested the surface lines to 125 bar/ 10 min. Attempted to pressure test surface cement plug below RTTS plug. Pressure broke at around 30 bar. Stopped pressuring up. Pressure leaked off." "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Released RTTS plug, POOH w/ RTTS BHA, losses 1,6m3/hour" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.8 hours. Operational details: L/D RTTS BHA, R/B 8,25in drill collars. Cleaned drill floor" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to N/D diverter" "On 2016-07-07, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Removed elevators and rotator. Attached chains to bails. Installed lifting eyebolts to diverter. Pulled diverter to rig floor, 11,5t overpull to come free.Installed outer ring and master bushing" "On 2016-07-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Pulled and secured diverter to setback. Cleaned bell nipple and removed bolts, prepared for lifting. Pulled bell nipple to rig floor, landed, installed outer ring and master bushing" "On 2016-07-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: TBT for rigging down tensioners, breaking NT2 and skidding BOP to stump. Transfered weight from tensioners to BOP carrier, removed and secured tensioners. Drop checked BOP prior to starting on NT2 connector." "On 2016-07-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Released NT2 connection" "On 2016-07-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Skidded BOP from well to stump" "On 2016-07-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: M/U BOP NT2 connection onto stump w/ 1600ft/lbs" "On 2016-07-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Prepared to pull riser, carried out TBT for pulling HP riser. Removed master bushing and outer ring. Installed handrails around rotary table. Lowered down TDS/Chains and attached slings to chain for pulling HP riser. Loosened last 4 bolts on riser and removed half-moon covers. Pulled Riser to rig floor and layed out same on HTS, 5.5t. Cleared rig floor." "On 2016-07-08, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Removed half-moon hatches from F-1 and moved them to moon pull. Installed hatch over F-1 slot. CONTINUED REPORTING ON F-15D It is planned to verify status of surface cement plug during riser removing work, upon completion of main PnA activities on other wells" "On 2016-09-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Prepared for skidding" "On 2016-09-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to skid cantilever" "On 2016-09-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.2 hours. Operational details: Skidded cantilever 3m to port and 10m forward" "On 2016-09-16, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Removed hatches in moon pool and performed afterskid checks" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Installed half moon cover in moon pool" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed and M/U HP riser" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Built scaffolding in moon pool. Meanwhile serviced TDS, installed cover in wellhead level" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Skidded BOP from stump to riser and landed same. Cleaned and inspected seal face" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: M/U NT2 connector and installed tension cylinder" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: N/U slick joint and diverter" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Alligned diverter and slick joint. M/U slick joint and removed lifting equipment from diverter. Installed elevator. Pressured up diverter system" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Filled the well using trip tank. Well not static" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared drill floor" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U cutter BHA (run#38)" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to RIH w/ cutter BHA" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Changed master bushing to PS21 slips" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 695m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: RIH from surface to 695m with cutter BHA (run#38). Average running speed 926 m/hour" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 695m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: M/U TDS and filled pipe. Took parameters: 400 l/min - 35 bar, 500 l/min - 57 bar, 600 l/min - 78 bar, 60 rpm - 1-4 kNm, 80 rpm - 1-5 kNm. Up weight 92t, down weight 88t" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 728m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cut 13 3/8in casing at 724.5m. 400 l/min - 35 bar - 60 rpm - 2-7 kNm. Increased to 500 l/min - 57 bar - 80 rpm - 6-11 kNm. Observed pressure drop from 57bar down to 22 bar and torque drop to free rotation torque. P/U out of cut and observed pressure increased to 57 bar. RIH and observed pressure dropped. Measured cut of 10 cm" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 728m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Circulated BU at 1000 l/min - 13 bar. No gas or H2S detected from gas trap" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 493m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH wet from 728 m to 493 m" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 493m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Installed mud bucket line" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Continued to POOH wet from 493m to 50m. Average pulling speed 460 m/hour" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Changed PS21 slips to master bushing" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: POOH from 50m to surface and L/D cutter BHA" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting P/U 13 3/8in EZSV plug (run#39)" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: P/U 13 3/8in EZSV plug BHA (run#39), M/U and installed spring centralizer" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 164m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH w/ 13 3/8in EZSV plug BHA (run#39) from surface to 164m, restricted to 2 min/stand" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 164m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21 slips" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 710m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH w/ 13 3/8in EZSV plug BHA (run#39) from 164 m to 710 m restricted to 2 min/stand" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 710m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed master bushing" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 720m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS and washed from 710 m to 720 m w/ 800 l/min - 5 bar" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Set EZSV at 715 m bottom plug. Sheared with 24t, Tagged with 5t and released stinger with 25 turns" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed 1.5m pup and cement assy, connected hose" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Performed integrity test against lower and upper FOSV on cement assy" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Performed pressure test below EZSV with cement unit. Failed" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Closed UPR and lined up to pump down kill line at 200 l/min - 30 bar whilst holding and monitoring 5 bar pressure on the cement unit. No pressure increase observed on cement unit. Confirmed hydraulic isolation of annulus cement plug behind 13 3/8in csg" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Opened UPR and lined up to pump wash pill" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 10m3 wash pill at 2500 l/min - 20 bar. Lined up to pump cement from cement unit" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Balanced cement plug (714 m - 614 m ): Mixed and pumped 7,8 m3 of 1,95 SG cement slurry, 600 l/min. Displaced the cement with 6,5 m3 of drill water. TOC 614 m" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 715m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/D cement hose and broke off cement assy. L/D same" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 550m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH from 715m to 550 m restricted 2min/ stand" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 550m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Installed sponge ball. Pumped sponge ball w/ 1800 l/min - 10 bar - 50 rpm" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 550m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Broke off TDS. Continued to POOH to 510m" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 510m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Opened elevator while not holding with PRS arm which resulted in loose stand of pipe in derrick. Secured stand. Checked upper PRS head" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 510m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Carried out TOFS" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 473m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Continued to POOH from 510M to 473M" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 473m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Installed BOP wash tool. Washed BOP w/ 1400 l/min - 12 bar 10 rpm. Performed 3x passed, functioned BOP and performed another 3x passed. L/D wash tool" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 30m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH from 473 m to 30 m. P/U single from HTS" "On 2016-09-17, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Inspected and L/D EZSV running tool" "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor. Meanwhile performed AAR" "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Prepared to N/D diverter system. Carried out TBT" "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: N/D diverter" "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Shifted load to BOP carrier. Removed tension cylinders and broke off NT-2 connector" "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lifted BOP. Skidded and landed BOP onto test stump" "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed scaffolding in moonpool. Meanwhile loosen HP riser on wellhead and prepared for to rig up bleed off manifold." "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed lifting gear on HP riser and lifted same to the drill floor" "On 2016-09-18, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Removed half moon hatch and installed hatch on F-1. Meanwhile prepared for skidding CONTINUE REPORTING ON F-11B" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding rig" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Skidded cantilever to well F-1 C" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Performed post-skid checks. Removed hatch in moonpool Built scaffolding in moonpool and WH decks." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U hoses for displacing riser to SW" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lowered down and N/U NT2 connector" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U and M/U cutter BHA and inner string. Inspected and cleaned threads on RT." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Engaged RT to Multibowl. Took 20 ton overpull to confirm. M/U TDS" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT to N/D tension system." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Load shifted weight from tension cylinders to TDS. Observed to increased weight on weight indicator." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Discussed plan ahead." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Displaced riser to SW by pumping 10 m3 SW at 100 lpm, return seen after 7 m3 pumped. Meanwhile: Prepared to R/D tension cylinders." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/D tension cylinders and boat collision stool. Meanwhile: Prepared to pull Multibowl to drill floor." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled 20 ton overpull. R/U return hoses to WH, secured same." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Staged up flow rate to 2400 lpm / 87 bar. Cut riser at 134,9m." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D return hoses and valve outlets from Multibowl." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with inner string and riser to drill floor. Disengaged Multibowl RT and R/B same in PRS." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U false rotary. POOH and R/B inner string and cutter BHA." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U Multibowl RT." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with riser, cleaned off marine growth on centralizer deck. Performed TBT for L/O Multibowl and tensioner joint." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 1,8m. R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: L/O Multibowl and tensioner joint. R/D NT2 connector and Multibowl RT. Meanwhile: Removed BX-elevator." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with riser (Lift #2). Cleaned off marine growth on centralizer deck." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U cutting machine Cut riser. Significant wave height 1,9 m. R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O splash zone joint and upper pup joint. POOH with riser (Lift #3)." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U cutting machine Cut riser. Significant wave height 1,5 m R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #3). POOH with riser (Lift #4). Cleaned off marine growth on centralizer deck. Riser out of splash zone at 20:30" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 1,5m R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #4). POOH with riser (Lift #5). Cleaned off marine growth on centralizer deck." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #5). POOH with riser (Lift #6). Cleaned off marine growth on centralizer deck." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine Cut riser. R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #6). POOH and L/O stress joint and lower pup joint (Lift #7)." "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-10-21, at Well NO 15/9-F-1 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed moon pool hatches and removed scaffolding. Meanwhile: Prepared to skid rig **** END OF REPORT ****" "On 2013-05-14, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 2586m MD to 2616m MD with 1600-2000 lpm, 102-123 bar, 60 rpm, 11-14 kNm, 3-6 MT, 1.33 sg ECD. Average ROP: 10 m/hr." "On 2013-05-14, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Experienced false fire alarm and ESD. Secured well and observed on trip tank. Restarted power supply to drilling systems and Baker unit. Observed hydraulic leak in top drive during power outage on rig floor." "On 2013-05-14, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly from 2616m MD to 2536m MD." "On 2013-05-14, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'interruption -- other' and lasted for 6.5 hours. Operational details: Inspected top drive for hydraulic leak. Repaired leaking connection on hydraulic hose. Meanwhile: Performed general maintanence and housekeeping." "On 2013-05-15, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'interruption -- maintain' and lasted for 3.5 hours. Operational details: Repaired leaking connection on hydraulic hose on top drive. Meanwhile: Performed general maintanence and housekeeping." "On 2013-05-15, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2576m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Held tool box talk prior to RIH. Installed PS-21 power slips. Ran in hole with 8 1/2' bottom hole assembly from 2536 m MD to 2576 m MD." "On 2013-05-15, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2617m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Washed down with 8 1/2' BHA from 2576 m MD to 2617 m MD with 1800 liter/min, 98 bar, 20 rpm, 7-10 kNm. Made up TDS and performed survey." "On 2013-05-15, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2617m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Recorded slow circulation rates." "On 2013-05-15, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2772m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 2617 m MD to 2772 m MD with 2400 liter/min, 102-123 bar, 140 rpm, 12-16 kNm, 4-6 MT, 1.36 sg ECD. Average ROP: 26 m/hr." "On 2013-05-15, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3000m. The activity was categorized as 'drilling -- drill' and lasted for 12.5 hours. Operational details: Drilled and oriented 8 1/2' hole from 2772 m MD to 3000 m MD with 2000-2400 liter/min, 109-179 bar, 140-180 rpm, 11-18 kNm, 4-11 MT, 1.352-1,373 sg ECD. Average ROP: 18 m/hr." "On 2013-05-16, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'drilling -- drill' and lasted for 19.5 hours. Operational details: Drilled and oriented 8 1/2' hole from 3000 m MD to 3302 m MD with 2160-2319 liter/min, 151-173 bar, 180-190 rpm, 13-27 kNm, 2-9 MT, 1.34-1,37 sg ECD. Average ROP: 15,5 m/hr." "On 2013-05-16, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.5 hours. Operational details: Performed survey at 3300 meter MD. Circulated 3 x bottoms up to clean hole with 1800-2300 liter/min, 165-173 bar, 120 rpm, 12-16 kNm, 1,36 sg ECD. Meanwhile: Prepared and rigged up for wireline job." "On 2013-05-17, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Continued to circulate hole clean with 1800-2300 liter/min, 165-173 bar, 120 rpm, 12-16 kNm, 1,36 sg ECD. Meanwhile: Prepared and rigged up for wireline job. Held pre-job meeting prior to wireline job." "On 2013-05-17, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Flow checked well, OK." "On 2013-05-17, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.0 hours. Operational details: Rigged up logging equipment. Made up CSES assembly and connected to TDS." "On 2013-05-17, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: RIH with gyro inside 5 1/2' DP string from surface to 2133 meter. Meanwhile: Moved string every 30 minutes. Monitored well on trip tank." "On 2013-05-17, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Closed wireline stuffing box. Pumped gyro down inside 5 1/2' DP string with 600-700 liter/min, 27-32 bar." "On 2013-05-17, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: Logged interval from 3144 m MD to 2580 m MD. Meanwhile: Moved string every 30 minutes. Monitored well on trip tank." "On 2013-05-17, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3302m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.0 hours. Operational details: Rigged down logging equipment. Broke out CSES assembly and disconnected from TDS." "On 2013-05-19, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3376m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3301 m MD to 3376 m MD with 2290 liter/min, 181-185 bar, 180 rpm, 17-21 kNm, 4-7 MT, 1.38-1,42 sg ECD. Average ROP: 25 m/hr." "On 2013-05-20, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3561m. The activity was categorized as 'drilling -- drill' and lasted for 10.5 hours. Operational details: Drilled and oriented 8 1/2' hole from 3376 m MD to 3561m MD with 2290 liter/min, 181-185 bar, 180 rpm, 16-19 kNm, WOB 2-7 MT, 1.39-1,45 sg ECD. Average ROP: 18 m/hr. At 3380 meter commenced weighing up mud system from 1,28 sg to 1,32 sg. At 05:00 hrs. restricted ROP to 15 meter/hr due to increase in ECD. Top Hugin formation at 3561 meter." "On 2013-05-20, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3646m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3561 m MD to 3646 m MD with 2290 liter/min, 185-189 bar, 180 rpm, 16-19 kNm, WOB 6-11 MT, 1.42-1,43 sg ECD. Average ROP: 17 m/hr. TDS not able to maintain rpm due to loss of power." "On 2013-05-20, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3646m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Worked with solving TDS power loss problem." "On 2013-05-20, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3749m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3646 m MD to 3749 m MD with 2290 liter/min, 189-191 bar, 180 rpm, 17-21 kNm, WOB 6-13 MT, 1.42-1,43 sg ECD. Average ROP: 13 m/hr. Experienced drilling braek at 3647 meter. Performed flow check for 15 minutes, well stable." "On 2013-05-21, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3762m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3749 m MD to 3762 m MD with 2290 liter/min, 189-191 bar, 180 rpm, 17-21 kNm, WOB 6-13 MT, 1.42-1,43 sg ECD. Average ROP: 13 m/hr. Obtained survey at TD." "On 2013-05-21, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3731m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Circulated hole clean with 1800 liter/min down and 2300 liter/min up, 130-188 bar, 125 rpm, 17- 19 kNm, 1,42 sg ECD. After 1 x bottoms up racked back 1 stand. Circulated total 3 x bottoms up." "On 2013-05-21, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3707m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Relogged interval from 3730 m MD to 3707 m MD with 2300 liter/min, 193 bar." "On 2013-05-21, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3707m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Performed sticky test with drill string static for 20 minutes, observed 5 Ton overpull. Meanwhile: Held pre-job meeting prior to taking pressure points." "On 2013-05-21, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3628m. The activity was categorized as 'formation evaluation -- log' and lasted for 10.0 hours. Operational details: Recorded pressure points in interval between 3711,5 m MD and 3596,3 m MD Total pressure points recorded, 19. Commenced waiting 48 hours prior to take new pressure points." "On 2013-05-21, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3005m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Waited prior to take new pressure points. Meanwhile: Pumped OOH with 8 1/2' BHA on 5 1/2' DP from 3628 m MD to 3005 m MD at 1000 liter/min, 42 bar, max speed 21 meter/min." "On 2013-05-21, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Waited prior to take new pressure points. Meanwhile: POOH with 8 1/2' BHA on 5 1/2' DP from 3005 m MD to 2494 m MD, max pulling speed 8 meter/min." "On 2013-05-22, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'interruption -- wait' and lasted for 3.0 hours. Operational details: Waited prior to take new pressure points. Meanwhile: Circulated bottoms up with 1000 liter/min, 36 bar. Cleaned and tidied on drillfloor. Prepared maintenance work on drilling equipment." "On 2013-05-22, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waited prior to take new pressure points. Meanwhile: Flow checked well, ok. Cleaned and tidied on drillfloor. Prepared maintenance work on drilling equipment." "On 2013-05-22, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'interruption -- wait' and lasted for 20.0 hours. Operational details: Waited prior to take new pressure points. Monitored well on trip tank. Meanwhile: Cleaned and tidied on drillfloor and in all drilling areas. Performed maintenance work on drawworks. Replaced Bypass Actuator Valve for downlink system. Worked with 5 yearly maintenance on stand pipe valve S6. Performed toubleshooting and maintenance jobs on TDS. Worked with installation of BHA Wash Tool control system. Circulated well every 6th hour with 1100 liter/min, 43-46 bar." "On 2013-05-23, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'interruption -- wait' and lasted for 12.0 hours. Operational details: Waited prior to take new pressure points. Monitored well on trip tank. Meanwhile: Cleaned and tidied on drillfloor and in all drilling areas. Worked with 5 yearly maintenance on stand pipe valve S6 and S9. Completed valve S6. Performed toubleshooting and maintenance jobs on TDS, VFD faults. Worked with installation of BHA Wash Tool control system. Circulated well every 6th hour with 1100 liter/min, 43-46 bar." "On 2013-05-23, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3746m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: RIH with 8 1/2' BHA from 2494 m MD to 3746 m MD. Filled pipe at 3020 meter." "On 2013-05-23, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3762m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Washed down from 3746 m MD to 3762 m MD with 2220 liter/min, 194 bar, 20 rpm, 13-17 kNm. Tagged bottom at 3762 m MD." "On 2013-05-23, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3762m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Circulated and conditioned mud with 2300 liter/min, 2160 bar, 100 rpm 16-20 kNm, max gas 0,43%. Performed sticky test with string static for 20 minutes, no overpull observed. Meanwhile: Held pre-job meeting prior to take pressure points." "On 2013-05-23, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3602m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: Recorded pressure points in interval between 3681 m MD and 3602 m MD Total pressure points recorded, 5." "On 2013-05-23, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2896m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: Pumped OOH with 8 1/2' BHA on 5 1/2' DP from 3602 m MD to 2896 m MD at 1000 liter/min, 48-50 bar." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2563m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Pumped OOH with 8 1/2' BHA on 5 1/2' DP from 2896 m MD to 2563 m MD at 1000 liter/min, 48-50 bar." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2563m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well for 15 minutes inside 14' casing shoe, static." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 182m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP from 2563 m MD to 182m MD at restricted speed due to swab simulations. Held pre-job meeting prior to change handling equipment." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 182m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Performed flowcheck prior to pull BHA through BOP. Changed handling equipment." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 8 1/2' BHA from 182 m MD to 45 m MD. Held toolbox talk prior to handle radioactive source." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed radioactive source." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Plugged into OnTrack and verifyed tool string." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH and laid down 8 1/2' BHA from 45 m MD to surface." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Cleaned and cleared drillfloor. Performed Pre-job meeting prior to rig up and run 3 1/2' DP stinger. Changed to 3 1/2' handling equipment." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2255m. The activity was categorized as 'drilling -- other' and lasted for 5.0 hours. Operational details: Made up and RIH with muleshoe on 3 1/2' from surface to 380 m MD. Changed to 5 1/2' DP handling equipment." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: RIH with 3 1/2' stinger on 5 1/2' DP from 380 m MD to 3200 m MD. Average tripping speed 940 meter/hour. Filled pipe at 2570 meters." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3762m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Connected TDS and washed down with 3 1/2' stinger from 3200 m MD with 500 liter/min, 30 bar, tagged bottom at 3762 m MD." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3754m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Laid out single. Made up side entry sub assembly with DPSV's." "On 2013-05-24, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3754m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Circulated and conditioned mud with 2400 liter/min, 233 bar, 60 rpm, 13-16 kNm, reciprocated pipe from 3754 m MD to 3720 m MD." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3754m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Circulated and conditioned mud with 2400 liter/min, 233 bar, 60 rpm, 13-16 kNm, reciprocated pipe from 3754 m MD to 3720 m MD. Stopped and flow checked well for 15 mintes at 01:15 hrs, well static. Performed pre-job meeting prior to cement job while circulating." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3754m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Pumped 13,3 m3 of 1,50 sg spacer with 800 liter/min, 39 bar. Mixed and pumped 13,2 m3 of 1,90 sg cement slurry with 650 liter/min. Displaced the cement to the rig floor with 890 liters of drill water. Pumped 1,8 m3 of 1,50 sg spacer with rig pumps. Zeroed volume counters. Displaced the cement with 31 m3 of 1,32 sg mud at 2500 liter/min, 132-247 bar, 30 rpm, 12-14 kNm." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3325m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Pulled out of cement to 3325 m MD. Theoretical TOC at 3484 m MD." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3325m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Installed two sponge balls. Circulated 1,5 x string volume with 2400 liter/min, 230 bar, 50 rpm, 10 kNm." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3080m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Waited on cement. Meanwhile: POOH wet with 3 1/2' stinger from 3325 m MD to 3080 m MD." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3040m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Waited on cement. Meanwhile: Circulated out remaining spacer with 2450 liter/min, 217 bar, 50 rpm, 11 kNm, reciprocated string from 3080 m MD to 3040 m MD. Observed spacer in returns." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2370m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Waited on cement. Meanwhile: POOH wet with 3 1/2' stinger from 3040 m MD to 2370 m MD. Cleaned and cleared drillfloor." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2370m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waited on cement. Meanwhile: Cleaned and cleared drillfloor. Removed PS-21 power slips and installed master bushings. Picked up and made up BOP test tool." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waited on cement. Meanwhile: RIH with BOP test tool from surface to 139,2 meter. Landed BOP test tool in wellhead." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- wait' and lasted for 6.5 hours. Operational details: Waited on cement. Meanwhile: Tested BOP pipe rams and annular preventers to 20 bar / 5 min and 345 bar / 10 min. Tested kelly hose, upper / lower IBOP's, kill and choke lines to 20 bar / 5 min and 345 bar / 10 min." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2370m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Waited on cement. Meanwhile: POOH with BOP test tool from 139,2 m MD to surface and laid down same." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3280m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waited on cement. Meanwhile: RIH with 3 1/2' stinger from 2370 m MD to 3280 m MD. Average tripping speed 910 meter/hour." "On 2013-05-25, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3280m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: Waited on cement. Meanwhile: Circulated and reduced MW from 1,32 sg to 1,28 sg with 2500-2941 liter/min, 225-282 bar, 61 rpm, 7-10 kNm, reciprocated pipe from 3280 m MD to 3242 m MD." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3280m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Circulated and reduced MW from 1,32 sg to 1,28 sg with 2500-2941 liter/min, 225-282 bar, 61 rpm, 7-10 kNm, reciprocated pipe from 3280 m MD to 3242 m MD." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 3389m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: RIH with 3 1/2' cement stinger from 3280 m MD to 3365 m MD. Established circulation and washed down from 3365 m MD to TOC at 3389 m MD with 500 liter/min, 25 bar. Tagged cement with 10 Ton." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2968m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: POOH wet with 3 1/2' stinger from 3389 m MD to 2968 m MD." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2968m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Spotted 10 m3 1,32 sg HI-Vis pill." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: POOH with 3 1/2' cement stinger on 5 1/2' DP from 2968 m MD to 2760 m MD. Circulated and conditioned mud with 2410 liter/min, 190 bar, 50 rpm, 6-8 kNm, reciprocated pipe from 2760 m MD to 2520 m MD. Performed pre-job meeting prior to cement job while circulating." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2760m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Pumped 22 m3 of 1,50 sg spacer followed by 1,3 m3 mud with 800 liter/min, 35 bar. Mixed and pumped 13,5 m3 of 2,00 sg cement slurry with 670 liter/min. Displaced the cement to the rig floor with 890 liters of drill water. Pumped 2,0 m3 of 1,50 sg spacer with rig pumps. Zeroed volume counters. Displaced the cement with 24 m3 of 1,32 sg mud at 2530 liter/min, 110-215 bar, 30 rpm, 5-8 kNm." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2500m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Checked for back flow, no back flow observed. Broke out and laid down pump in assembly. POOH with 3 1/2' cement stinger on 5 1/2' DP from 2760 m MD to 2500 m MD. Installed two sponge balls. Circulated bottoms up with 2660 liter/min, 222 bar, 60 rpm, 6-8 kNm. Observed traces of cement, diverted 68 M3 interface to slop pit." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2500m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Flow checked well, static. Pumped slug." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 380m. The activity was categorized as 'drilling -- other' and lasted for 4.5 hours. Operational details: POOH with 3 1/2' cement stinger on 5 1/2' DP from 2500 m MD to 380 m MD. Average tripping speed 471 meter/hour." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: POOH and laid down 3 1/2' cement stinger from 380 m MD to surface." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Rigged down 3 1/2' handling equipment. Cleaned and cleared rigfloor. Function tested blind shear ram." "On 2013-05-26, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Performed pre-job meeting prior to pick up BHA. Picked up 12 1/4' drilling BHA and RIH." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 14m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Picked up 12 1/4' drilling BHA and RIH to 14,3 meter. Observed hydraulic leak on TDS, stopped operation." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 14m. The activity was categorized as 'interruption -- other' and lasted for 9.0 hours. Operational details: Replaced faulty alignment cylinder on TDS. Meanwhile: Prepared to rig up handling equipment for pick up and rack casing. Held pre-job meeting prior to pick up 12 1/4' BHA." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Picked up 12 1/4' drilling BHA and RIH from 14,3 m MD to 32,3 m MD. Baker plugged into ON TRACK. Unable to get contact between Co-pilot and ASS. Troubleshooted and replaced TSC box." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 93m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA on 6 5/8' HWDP from 32,2 m MD to 93 m m MD. Removed masterbushings and installed PS-21 power slips." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 207m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Picked up and broke out connection between accelerator and HWDP, installed Totco ring. Made up connection and continued to RIH with 12 1/4' BHA on 6 5/8' HWDP from 93 m MD to 207 m MD. Observed leak on TDS, stopped operation." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 207m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Discovered leak on TDS oil cooler, isolated hydraulic system and dismantled cooler." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 207 m MD to 2494 m MD. Filled pipe every 1000 meters. Average tripping speed 508 meter/hour." "On 2013-05-27, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Performed choke drill. Observed hydraulic oil leak on TDS, stopped operation." "On 2013-05-28, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2494m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Isolated TDS hydraulically. Repaired leaking hydraulic pipe fitting and installed overhauled hydraulic cooler." "On 2013-05-28, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Washed down with 12 1/4' BHA from 2494 m MD to TOC with 1450-3400 liter/min, 27-168 bar, 90-170 rpm, 6-12 kNm, WOB 0-8 Ton. Observed hard cement at 2531 m MD" "On 2013-05-28, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2575m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled cement from 2531 m MD to 2575 m MD with 2807 liter/min, 164-168 bar, 155 rpm, 9-13 kNm, WOB 6-13 MT." "On 2013-05-28, at Well NO 15/9-F-11 A, a drilling event occurred at a depth of 2627m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled cement and new formation with restricted ROP 5 meter/hour from 2575 m MD to 2627m MD with 2807 liter/min, 164-168 bar, 155 rpm, 9-13 kNm, WOB 6-13 MT. At 11:30 hrs observed 50% new formation in returns. At 14:30 hrs observed 100% new formation in returns. Continue reporting on well F-11 B." "On 2009-01-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2579m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 12 1/4' hole section from 2575 m to 2579 m MD. Drilling parameters : 3000 lpm / SPP~160 bar / 80 rpm / Torque~16 kNm / WOB 1-3 MT. Controlled ROP to 2 m/hrs (time drililling). Routed returns to bigbag/IBC due to washout in DCI piping." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2585m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled and oriented 12 1/4' section from 2579 m to 2585 m MD. Drilling parameters : 3000 lpm / SPP ~157 bar / 130 rpm / Torque ~18 kNm / WOB ~2 MT. Controlled ROP to 2 m/hrs (time drililling). Routed returns to skips due to washout in DCI low pressure piping." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2585m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Pulled back into at 2545 m MD. As permitted by weather condtions, performed ciritical maintenance of TDS and PRS. Disconnected hose on cement standpipe for troubleshooting blockage on hose. Meanwhile perfomed cleaning of DCI mill tank." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2585m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Excess time used on service on TDS and PRS. RIH to TD at 2585 m MD." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Downlinked Powerdrive. Drilled and oriented 12 1/4' section from 2585 m to 2590 m MD. Drilling parameters : 3000 lpm / SPP ~160 bar / 130 rpm / Torque ~20 kNm / WOB ~1-5 MT / ECD 1,28. Controlled ROP to 10 m/hrs as dictated logistic challenges / weather conditions. Meanwhile performed cleaning/repairs in DCI system." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2663m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: Drilled and oriented 12 1/4' hole section from 2590 m to 2663 m MD. Drilling parameters : 3000 lpm / SPP ~160 bar / 80-130 rpm / Torque 20-24 kNm / WOB 2-7 MT / ECD 1,29. Stepped up ROP in incrememts from 10 to 25 m/hrs as dictated by cuttings handling." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2663m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: At 2663 m MD, got problems with Powerdrive - not able to maintain toolface/steering. Pulled out to 2654 m MD and downinked Powerdrive in attempt to regain steering." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2665m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled ahead to 2665 m MD - prevailing problems in maintaining toolface with Powerdrive." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2665m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Reciprocated on stand whilst discussing situation with town. Decided to POOH to change Powerdrive." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2665m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well prior to POOH - well static." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2665m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 5 m3 1,57 sg slug. Allowed mud level to settle." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2464m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 12 1/4' drilling BHA on 5 1/2' DP from 2565 m to 2464 m MD. Open hole tripping speed 200 m/hrs." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 609m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH with 12 1/4' drilling BHA on 5 1/2' DP from 2464 m to 609 m MD. Tripping speed 1280 m/hrs." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 609m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked prior to pulling BHA - well static. Observed slack hoist wire on PRS." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 609m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Troubleshot slack wire on PRS. Found mismatch on tension cyclinders - rectified problem." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 12 1/4' drilling BHA on 5 1/2' HWDP from 609 m to 107 m MD." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for installing bushings." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed auto slips. Installed masterbushing and bowl." "On 2009-01-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH with 12 1/4' BHA. Racked back BHA in derrick. Broke out powerdrive. Broke bit using rig tongs." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Laid down Powerdrive. Picked up back-up Powerdrive. Made up 12 1/4' bit. Hung off powedrive in rotary." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Made up and RIH with 12 1/4' BHA to 107 m MD." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed masterbushing. Installed auto slips." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 606m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' HWDP/DP from 107 m to 606 m MD." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 606m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Fiilled pipe and performed shallow test of Powerdrive and MWD - ok. Performed kick-drill." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1697m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 606 m to 1697 m MD. Filled pipe every 500 m tripping in. Tripping speed 545 mhrs." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2626m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 1697 m to 2626 m MD. Filled pipe every 500 m. Tripping speed 465 m/hrs." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2665m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Made up TDS. Washed down last stand at 2000 lpm / SPP 80 bar." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2755m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled and oriented 12 1/4' hole section from 2665 m to 2755 m MD. Downlinked Powerdrive and took surveys at connections as instructed by DD/MWD. Drilling parameters : 3200 lpm / SPP ~180 bar / 65-130 rpm / Torque 18-24 kNm / WOB 2-8 MT / ECD 1,28. Linited ROP to 10 m/hrs due limited processing capacity and ongoing work on DCI. Full capacity of DCI regained at 18:00." "On 2009-01-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2790m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and oriented 12 1/4' hole section from 2745 m to 2790 m MD. Drilling prameters : 3200-3400 lpm / SPP 175-195 bar / 130 rpm / Torque 18-24 kNm / WOB 2-9 MT / ECD 1,27. ROP 3-8 m/hrs as determined by geology. Experienced high stick/slip and low ROP from ~2770 m MD (Ekofisk). 100% limestone shows at 2780 m MD. Performed kick drill." "On 2009-01-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2818m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and oriented 12 1/4' hole section from 2790 m to 2818 m MD. Drilling parameters 3400 lpm / SPP ~180 bar / 130-160 rpm / Torque 20-26 kNm / WOB 5-9 MT / ECD 1,27. ROP 2-8 m/hrs as determined by geology. Experienced high stick/slip when drilling chalk." "On 2009-01-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2853m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: Drilled 12 1/4' hole section from 2818 m to 2853 m MD. Drilling parameters : 3400 lpm / SPP ~194 bar / 150-180 rpm / Torque 23-29 kNm / WOB 10-12 MT / ECD 1,27. ROP 3-8 m/hrs as determined by geology and stick/slip. Lost return flow and standpipe pressure." "On 2009-01-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2827m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Observed lost return to pit and falling standpipe pressure. Picked off bottom and reciprocated stand from 2827 m to 2841 m MD / 10 rpm. No drop in active, annulus full, i.e. no downhole losses detected. Ivestigated situation. Inspected lines from pit to TDS, found no leakages. Closed IBOP and attmepted to pump, found that problem was related to the surface system." "On 2009-01-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2827m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Lined up cement unit to circulate on well. Circulated in well at set intervalls using cement unit pumping at 1200 lpm / SPP 26 bar. Reciprocated stand and rotated 10 rpm. Monitoed well on trip tank when not pumping - well static. Performed troubleshooting on pumps and circulation system." "On 2009-01-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2853m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Found likely cause of problem to be blocked splitter valve in suction module. Not able to use pit#7 as active pit. Lined up to pump from pit #15 taking retuns to pit #15 and #7 and used mixpump for levelling the two pits. Stepped up pumprate to 3400 lpm and RIH to 2853 m MD." "On 2009-01-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2865m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled 12 1/4' hole section from 2853 m to 2865 m MD. Drilling parameters : 3400 lpm / SPP ~194 bar / 150-180 rpm / Torque 24-27 kNm / WOB 6-8 MT / ECD 1,28. ROP 2-6 m/hrs as determined by geology." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2896m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole section from 2865 m to 2896 m MD. Drilling parameters : 3400 lpm / SPP ~198 bar / 150-180 rpm / Torque 24-27 kNm / WOB 6-8 MT / ECD 1,28. ROP 4-7 m/hrs as determined by geology." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled 12 1/4' hole from 2896 m to section TD at 2920 m MD. Drilling parameters : 3400 lpm / SPP ~195 bar / 180 rpm / Torque 28-32 kNm / WOB 3-5 MT / ECD 1,28. ROP 4-7 m/hrs as determined by geology." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.2 hours. Operational details: Circulated hole clean prior to POOH, reciprocated string between 2920 m and 2908 m MD. Parameters : 3400 lpm / SPP ~199 bar / 150 rpm / Torque 22-26 kNm / ECD 1,28." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flow checked well - static." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2904m. The activity was categorized as 'drilling -- survey' and lasted for 3.2 hours. Operational details: Broke off TDS. Dropped gyro. Made ut TDS and pumped gyro down string. Observed mud leakage from TDS, washpipe leaking. Pumped 5 m3 1,55 sg slug. Performed rotational gyro survey as instucted by Gyrodata." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2545m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 2904 m to 2545 m MD." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2545m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: Secured well with kelly cock-. Lowered TDS work platform. Changed washpipe. Installed test swadge on TDS." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2545m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Tested washpipe and standpipe to 345 bar / 10 min - ok. Broke swadge." "On 2009-01-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1132m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Filled trip tanks. POOH with 12 1/4' drilling BHA on 5 1/2' DP from 2545 m to 1132 m MD. Tripping speed 565 m/hrs. Meanwhile mounted riser cradles and laid out casing." "On 2009-01-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 12 1/4' drilling BHA on 5 1/2' DP from 1132 m to 109 m MD. Tripping speed 455 m/hrs. Meanwhile mounted riser cradles and lifted riser tension jonit / pup joint to cradle." "On 2009-01-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Flowchecked prior to pulling BHA - well static. Checked dies on PRS. Held toolbox talk for manual handling. Removed PS-21 auto slips. Installed masterbushing and bowls." "On 2009-01-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 12 1/4' BHA from 109 m MD to surfcae. Broke stand of 5 1/2' HWDP for acccess to gyro. Retrieved gyro. Made up HWDP stand and racked back same. Broke and racked back jar/DC stand in derrick. Broke and laid out 2 ea NMDC. Broke and laid out ARC, MWD and Powerdrive Xceeed." "On 2009-01-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleared and tided drilfloor. Lifted BHAs to baskets on maindeck." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 357m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 9 5/8' 53,5# 13Cr80 VamTop HCNA casing from 300 m to 357 m MD. Installed centralizers. Filled casing every 5th joint with OBM." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 357m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 9 5/8' 53,5# 13Cr80 VamTop HCNA casing from 357 m to 460 m MD. Installed centralizers. Filled casing every 5th joint." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 714m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 9 5/8' 53,5# 13Cr 80 VamTop HCNA casing from 460 m to 714 m MD. Filled casing every 5th joint with OBM." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 702m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rejected make-up of joint #47. Broke out joint - inspected and found damage on pin and box threads. Laid out joint #47. Broke and laid out joint #48." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 783m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 9 5/8' 53,5# 13Cr 80 VamTop HCNA casing from 702 m to 783 m MD. A 9 5/8' joint unexpectedly tilted off of the HTS roller section." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 795m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Held time out for safety and troubleshoting after a 9 5/8' casing joint was driven off of the HTS power rollers. Made up and ran 9 5/8' casing joint on HTS, installed swadge and kelly cock. Investigated incident. The 9 5/8' was tilted resting on the roller frame and the deck. The area in which the casing joint tilted was barriered off according to standard procedure for running HTS/PDM. Revised practice for picking up casing until further notice, i.e. only one joint on HTS rollers and HTS at the time." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 795m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk for continued casing running." "On 2009-01-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1113m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RIH with 9 5/8' 53,5# 13Cr 80 VamTop HCNA casing from 795 m to 1113 m MD. Filled casing every 10th joint with OBM." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1113m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Dressed PDM for picking up 10 3/4' casing. Changed to 10 3/4' BX4 elevator. Changed inserts in PS-21. Dressed tong for 10 3/4' casing. Moved roller section from forward to aft cantilever. Made up 10 3/4' swadge to kelly cock. Moved redundant 9 5/8' casing to fwd stb bay. Counted 9 5/8' joints left on deck, 37 - ok." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1580m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Made up 9 5/8' x 10 3/4 x-over. RIH with 10 3/4' 60,7# 13Cr80 VamTop casing from 1113 m to 1580 m MD. Filled every 10th casing joint with OBM." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1700m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2001m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 10 3/4' 60,7# 13Cr80 VamTop casing from 1700 m to 2001 m MD. Filled every 5th casing joint with OBM." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2001m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Removed power rollers on cantilever. Cleared excess equipment from drillfloor prior to running casing stands from derrick." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2001m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to running 10 3/4' casing stands." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2001m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Attempted to latch BX elevator onto casing stand in PRS - negative. Troubleshot. Decided to change to spider elevator." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2001m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Rigged down BX4 elevator and bails. Rigged up 15 ft bails. Made up FAC tool to TDS. Installed and hooked up spider elevator." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2001m. The activity was categorized as 'interruption -- other' and lasted for 3.8 hours. Operational details: Function tested spider elevator. Observed air supply problem from TDS. Troubleshot problem. Changed 2 way pneumatic valve on TDS." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2001m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk for running 10 3/4' casing stands." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2560m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: RIH with 10 3/4' casing stands from 2001 m to 2560 m MD. Filled every stand with OBM." "On 2009-01-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2560m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Stabbed 10 3/4' FAC packer into casing with 8 MT setdown. Commenced pumping, mud sprayed accross packer, not holding pressure. Set down 15 MT on FAC packer. Stepped up rate to 1330 lpm / SPP 31 bar. Circulated for 10 min, stable pressure and no losses. Took up/down weights 256/199 MT." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 10 3/4' casing stands from 2560 m to 2770 m MD. No significant drag in open hole (max 5 MT). Filled every stand with OBM." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging down equipment." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Removed PS-21 slips and installed masterbushing. Rigged down FAC tool. Rigged down spider elevator. Removed 15 ft bails and installed standard bails. Installed and hooked up DP elevator and link tilt. Counted 10 3/4' joints on deck, 9 ea - ok." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 10 3/4' casing hanger with elevator and tugger. Made up 10 3/4' casing hanger. Checked casing hanger according to Vetco procedure." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2779m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Ran 10 3/4' casing hanger below rotary and hung off on slips. Rigged down casing tong." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2779m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rigged dowm and removed Odfjell casing tong." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2779m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2779m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed excess casing handling equipment from drillfloor." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2911m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 9 5/8' x 10 3/4' casing on 5 1/2' HWDP from 2779 m to 2911 m MD. No siginificant drag in well. Filled pipe with OBM." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2911m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Connected hydraulic control lines and cement hose to cement head. Picked up and made up cement head. Made up cement hose to manifold outlet. Hooked up valve control panel. Made up TDS to cement head." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Staged up pumps in 200 lpm increments to 1500 lpm / SPP 57 bar. Washed down from 2911 m to 2915 m MD. Landed 10 3/4' hanger at 140,1 m MD and set down 5 MT. Verified measurements and set down 120 MT." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated bottoms up at 1500 lpm / SPP 57 bar. Meanwhile held toolbox talk for cement job." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up to cement unit. Pressure tested cement line and hose against lo-torq on cement head - 345 bar / 10 min - ok." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped 8 m3 of base oil at 1500 lpm / SPP 42 bar." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pumped 19 m3 1,3 sg cement spacer at 500 lpm and chased same with 2,5 m3 OBM. Released lower dart." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Mixed and pumped 1,9 sg silica cement at 800 lpm / CUP~55 bar. After pumping approx 15 m3 got problems with bulk transfer, not able to transfer from bulk tank#10 to surge tank." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot bulk transfer system. Pressured up on bulk tank#9. Meanwhile pumped cement at slow rate." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Transferred cement from bulk tank #9 to surge tank. Mixed and pumped rest of cement, in total 21,2 m3 1,9 sg silica cement." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced cement line partly with 500 l drillwater. Released upper dart and pumped another 1500 l drillwater from cement unit." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Lined up to use rigpumps for displacement. Zeroed stroke counter. Displaced cement at 1500 lpm / SPP 25-85 bar. Reduced pumprate to 1000 lpm after pumping 5288 strokes. Bumped plug after 5428 strokes with 147 bar (FCP 70 bar). Pump efficiency 96,7 %." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Closed IBOP and lined over to cement unit. Equalised across lo-torq with 160 bar. Pressured up to test casing 345 bar / 10 min. Observed pressure increasing 3 bar over 10 min due to thermal expansion of mud." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Bled back to cement unit to check for backflow. Bled back 2,2 m3 OBM. Observed pressure increase of 0,5 bar / min when shutting in. Bled back and measured return rate to 1,5 l/min. Suspected small leak across float valves." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Pressured up to 50 bar in order to equalise u-tube pressure from cement coulmn and stop back flow. Closed lo-torqe valve on cement head and disconnected cement hose. Flushed surfaced lines. Connected cement hose to cement head." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Equlalised across lo-torque valve on cement head with 60 bar. Opened lo-torq and read 71 bar in well. Bled back 650 liter, no continued backflow observed." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Disconnected cement hose and hydraulic control lines. Released PADPRT from 10 3/4' casing hanger with 8 clockwise turns. Pulled back to 137 m MD, broke and laid down cement head. Dropped 2 ea sponge balls, wiped and cleaned string pumping at 3300 lpm / SPP 33 bar for 10 min." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Laid out 2 ea 5 1/2' HWDP singles. POOH with PADPRT on 5 1/2' HWDP to surface. Broke and laid out PADPRT." "On 2009-01-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 87m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Made up setting tool / 10 3/4' lock down sub. RIH with lock down sub on 5 1/2' DP from surface to 87 m MD." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with lock down with lock down sub from 86 m to 140 m MD. Set lock down sub according to Vetco precdure. Pull tested lock down sub with 50 MT overpull - ok." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with lock down sub setting tool from 140 m MD to surface. Laid down setting tool." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 547m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with 6 stand of 5 1/2' HWDP from surface to 226 m MD. Made up 10 3/4' RTTS. RIH with RTTS to ~319 m MD." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 547m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up TDS, Set RTTS by clockwise rotation and set down 20 MT. RTTS set with mid packer element at ~319 m MD." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 547m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up from cement unit to pump through TDS. Put 10 bar pressure on IBOP, opened same and verified line-up. Pressure tested RTTS and casing below to 210 bar / 10 min - 0,3% drop - ok." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 541m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released from RTTS according to Halliburton procedure. Picked up to 313 m MD. Pressured up to 30 bar above RTTS." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 314m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Pressure tested RTTS / 10 3/4' casing above and cement in 9 5/8' x 13 3/8' annulus. Pressured up in 30 bar increments. Pressure dropped 1,5-2,5 bar / 10 min at 30, 60, 90 and 120 bar - but with improving trends towards end of each test. Continued to pressure up to 150, 180 and 210 bar and observed continued improving trend. Obtained test 210 bar / 10 min with 0,9 bar drop (0,42%) - ok. Bled off pressure and opened pipe ram. RIH with RTTS stinger to 314 m MD." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 314m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Staged up pumps and circulated bottoms up at 2000 lpm / SPP 9 bar." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 314m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Displaced from OBM to seawater above RTTS pumping at 2000 lpm / SPP 13-6 bar. Pumped in total in total 76 m3 seawter. Routed contamianted returns to pits. Flushed choke and kill lines with seawater." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 316m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Spotted 5 m3 hivis on top of RTTS." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 46m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: POOH with RTTS setting tool on 5 1/2' DP from 314 m to 46 m MD. Rigged up air line to choke manifold. Closed upper pipe tram. Purged air trhough choke/kill line taking returns via hose to mudbucket drain. Repeated purging." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with RTTS setting tool from 46 m MD to surface. Broke and laid out tool. Cleared and tidied drillfloor." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolboox talk prior to nippling diverter and BOP." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Rigged up long sling in TDS. Pulled diverter and set back on drillfloor." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Broke overshot connection on BOP. Pulled and set back overshot." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Nippled down BOP. Unable to break NT-2 studs on connector, adjusted BOP trolley accordingly. Not able to run BOP trolley due to hydraulic oil overheating." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot problem with hydraulic oil overheating. Ran other hydraulic equipment to cool hydraulic oil in main system." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Continued to nipple BOP connector. Could not break NT-2 studs, adjusted BOP trolley accordingly. Overtorqued and broke 1' x 3/4' x-over from j-gun to socket." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Searched rig for spare x-over / socket. Welded 1,5' hex socket onto 1' drive interface on j-gun. Meanwhile positioned Claxton tool and brought riser spider to drillfloor." "On 2009-01-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Broke NT-2 connector on BOP." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Broke NT-2 connector on BOP. Moved BOP to stb side using trolley. Landed BOP on stump." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Removed long slings from TDS. Installed bails and elevator. Removed master outer ring and master bushing. Ran Claxton tool through rotary using tugger. Installed outer ring and master bushing. Hung off Claxton tool on pup joint." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up stand of 5 1/2' DP to Claxton tool. Ran in with Claxton tool and landed same onto BOP joint." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up studs on Claxton tool to 3300 ft lbs." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up studs on Claxton tool to 3300 ft lbs." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Bled of hydraulic pressure on tension cylinders and transferred 60 MT tension to block. Retracted tension cylinders." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Dismantled contact ring and tensioner assembly. Removed centralizer in Centralizer deck. Landed tension ring on vinyl guide. Inserted wooden chuks in deck openings." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Rigged down scaffolding on Weather deck. Ran tugger line to seabed and attached same, ran hotstab to seabed. Issued instruction for shut-in on wells F-14, F-4 and F-5." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled dummy hotstab and engaged hotstab in TBC using ROV." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- wait' and lasted for 1.0 hours. Operational details: Waited on production to shut in and bleed off wells F-14, F-4 and F-5." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 128m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Adjusted blockweight to 110 MT / set down 20 MT. Applied 3000 psi unlock pressure to TBC. Observed indicator movement on ROV. Pulled riser free of wellhead in one continuous stroke. Pulled out and hung off in slips on Claxton pup joint." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 128m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Broke stand of 5 1/2' DP from Clacton tool. Made up stand of 5 1/2' DP to production riser running tool and racked back in derrick." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 126m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed master bushing and outer ring." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held toolbox talk for installing riser spider. Splitted, installed , hooked up and functioned riser spider. Pull out with HPDR to upper pup / tension joint connection. Removed fairings, hung off riser in spider." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Removed thread protectors. Broke flange according to Vetco procedure using Bandak bolt tensioner tools." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Laid out 1st double with simultaneous lift by block and deck crane. Adjusted slings to balance lift. Laid 1st double on riser m/u cradle." "On 2009-01-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Pull out with HPDR 2nd double 'D' 'and hung off in riser spider. Removed fairings. Removed thread protectors. Broke flange according to Vetco procedure using Bandak bolt tensioner tools. Made up handling flange type C using j-gun." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Laid out 2nd double 'D' by simultaneous lift by block and deck crane. Laid 2nd double in port riser rack." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pull out with HPDR 3rd double 'C' and hung off in riser spider. Removed fairings. Removed thread protectors. Broke flange according to Vetco procedure using Bandak bolt tensioner tools. Made up handling flange type C using j-gun." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Laid out 3rd double 'C' by simultaneous lift by block and deck crane. Laid 3rd double in port riser rack." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pull out with HPDR 4th double 'B' and hung off in riser spider. Removed fairings. Removed thread protectors. Broke flange according to Vetco procedure using Bandak bolt tensioner tools. Made up handling flange type C using j-gun." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Laid out 4th double 'B' by simultaneous lift by block and deck crane. Laid 4th double in port riser rack." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled out with HPDR 5th double 'A' (singel/stress/TBC)." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Laid out 5th double 'A' by simultaneous lift by block and deck crane. Laid 5th double in port riser rack." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared and tidied drillfloor and wellhead. Covered hatch on Centralizer deck. Prepeared for transferring tension cylinders to Centralizer deck." "On 2009-01-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Brought thension cylinders to Centralizer deck -Replaced tension cylinders -Changed wire on drillfoor yellow and black tugger -Trobleshot HTS - no clear fault indication - random behaviour at w.r.t. stop point -Performed maintenance of drawwork -Emptied pit #5 into skips" "On 2009-01-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Emptied pit#5 into skips -Perfromed NDT on drilling equipment -Changed oil on TDS -Greased C/K manifold -Tidied wellhead module -ROV brushed, cleaned and inspceted F-15 wellhead" "On 2009-01-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Waited on weather to run production riser. Wind checks performed on rig floor, cantiliver and derrick. Meanwhile : -Cleared centralizer deck and brought thension cylinders down. -Cleared rig floor to access TDS. -Inspected gasket on BOP stump and landed BOP. -MU NT2 connector on BOP stump. Opened BOP for 3 montly PM. -Mixed and injected slop in F-14. -Trouble shot on pipe handler (HTS) alignement. -Performed NDT on drilling equipment. -Brought tension cylinders up." "On 2009-01-31, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Performed NDT on drilling equipment. -Re-landed and MU NT2 connector on BOP stump. Prepared for pressure testing BOP. -Finished trouble shooting on pipe handler (HTS) alignement. -Removed tension sylinders from rig floor. -Removed riser spider and installed master bushings to access iron roughneck. -Started to disassemble aft iron roughneck. -Performed maintenace on kill and standpipe manifolds." "On 2009-01-31, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Instructed used of deluge/foam system on wellhead to crew as a part off weekly drill. -Pressure tested BOP on stump. Ok. -Disassembled and moved aft iron roughneck. -Disconnected fwd iron roughneck and moved to aft position. -Installed iron roughneck in aft position. -Installed two-part nylon protector guides and tension ring on F-15. -Vibration tested slurry pump." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Function tested iron roughneck in aft position. -Cleaned lower shakers. -RU to run tuggers through F-10 opening on centralizer deck. -Worked on motor for slurry pump. -Removed master bushings. Installed and function tested riser spider. -Built scaffolding/barriers around deck openings." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk for running production riser and hot-stab with involved personnel." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lifted TBC/stress joint from cantiliver until handling sub was latched into TDS. Unhooked uppermost sling and lifted TBC/stress joint with TDS until it was hanging vertically. Lifted hot-stab to drill floor. Meanwhile installed VX-ring using ROV." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Function tested TBC according to Vetco instructions." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Function tested TBC according to Vetco instructions." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: Waited on weather to run production riser. Informed Production to shut down F-4, F-5 and F-14 at 08:10. Meanwhile : -Performed rig maintenace -Routed tuggers to guide TBC/production riser." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk prior to running production riser. Lowered TBC/stress joint through rotary. Extended riser spider dogs and installed stop bolts in PR holes #3. Hung off stress joint in riser spider. Alligned TBC ROV panels and checked TBC connector for damage." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lifted 1st double with dual lift on block and deckcrane." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Disconnected handling tool. Made up flanged connection according to Vetco/Bandak procedure. Installed fairring on coupling. Ran in and placed TBC connector in level with Weather deck deck. Prepared guidewires in slot F-10. Ran and attched 10 MT guide wire to template. Attempted to run 6 MT guidewire, but the wire tangled around 10 MT tugger wire and slipped out of ROV hook assy, due to high winds. Waves had increased to 4-6 m and operation was stopped. Hung off PR in riser spider and kept TDS engaged to handling tool." "On 2009-02-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.0 hours. Operational details: Waited on weather to run production riser. Informed Production to re-start wells at 15:05. Meanwhile : -Performed rig maintenace -Performed derrick inspection/PM's in derrick. -Assembled slurry pump. -Cleaned lower shakers -Performed 3-yearly maintenace on valve C3 -Finished function test of iron roughneck" "On 2009-02-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Performed rig maintenace -Performed NDT on drilling equipment -Performed 3-yearly maintenace on valve C3 -Cleaned lower shakers -Installed rollers on PRS lower arm" "On 2009-02-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Performed 5-yearly maintenance on choke manifold (C13 and C16) -Performed maintenance on slips. -Performed maintenace on drag chain on main deck. -Cleaned lower shakers -Changed rollers on aft PRS -Trouble shot E-stop on fwd iron roughneck" "On 2009-02-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Performed 5-yearly maintenance on choke manifold (C13 and C16) -Cleaned lower shakers -Installed flush joint on aft PRS -Performed NDT on drilling equipment -Emptied water from below BOP NT2 connector" "On 2009-02-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Waited on weather to run production riser. Meanwhile : -Performed 5-yearly maintenance on choke manifold; C16 -Cleaned lower shakers -Re-arranged the half-moon hatches in moonpool to avoid hanging up when RIH with PR -Cleaned and backloaded lifting eyes for BOP -Replaced hang-off supporters for flowline on XMT deck -Cleared rig floor off flush joint elevators, cherry picker, slings etc -Performed NDT on drilling equipment -Errected scaffolding around moonpool hatches" "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waited on weather to run production riser. Informed Production to shut down F-4, F-5 and F-14 at 01:35 hrs. Meanwhile : -Performed 5-yearly maintenance on standpipe manifold; C8 -Cleaned lower shakers -Recovered moonpool 10 MT tugger from seabed -Held tool box meeting for untangeling guide wires and running PR" "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH 5-10 m with PR. Untangled 6 mT guide wire and hot-stab rope. Disconnected guide wire clamp from TBC. RIH and hung off PR in riser spider." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed handling tool. Lifted 2nd double to drillfloor with dual lift on block and deck crane. MU up flanged connection according to Vetco/Bandak procedure. Tested flanges to 3000 psi / 5 min, ok. RIH with PR from 37 m to 66 m through splash zone." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed handling tool. Lifted 4nd double to drillfloor with dual lift on block and deck crane. MU up flanged connection according to Vetco/Bandak procedure. Tested flange to 3000 psi / 5 min, ok. RIH with PR from 66 m to 118 m t." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed handling tool. Lifted tension joint double to drillfloor with dual lift on block and deck crane. MU up flanged connection according to Vetco/Bandak procedure. Attempted to pressure test flange to 3000 psi / 5 min." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pumped up pressure several times to obtain good test on tension joint double flange. Tested flanges to 3000 psi / 5 min, ok." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk with new crew prior to RIH with PR. RIH with tension joint double and landed off in riser spider." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Removed handling tool from riser tension joint. Observed lateral movement on flange studs. Verified with town prior to continued operation." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: MU pre-made landing stand to riser tension joint. MU TDS to landing stand. Meanwhile removed hole cover from RGLF and inspected ring gasket." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Lifted PR string, removed landing plate from tenion joint and lowered it down to top of riser landing guide funnel (RLGF). Hook load 97 mT. Continued lowering PR until TBC was 10 cm above VGX gasket. Removed RLGF and oriented TBC ROV panels. Landed TBC and sat down 15 mT weight. Launched hotstab down to seabed, attached to guidewire. Removed dummy hot stab and installed hydraulic hot stab into receptacle at top of TBC using ROV." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Sat TBC ROV panel A in 'primary unlock' 2-1-1 and RIH with PR another 10-15 cm. Sat TBC ROV panel A in 'primary lock' 2-1-2. Sat down 15 mT on PR. Pressured up through TBC port A to 3000 psi and observed silver band alignement of indicator rods above TBC top cap. Silver band was completely aligned. Sat TBC ROV panel A in 'parked position'. Production to re-start F-4, F-5 and F-14 at 18:00." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed 10 mT overpull test to 110 mT to confirmed that TBC was locked. Ok. Sat TBC ROV panel B in 'lower dog flush' x-1-1 and removed dummy hot-stab to be able to observe possible leak." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk and lined up to pressure test PR against RTTS plug from cmt unit using SW. Pressured up 15 bar against upper IBOP, but were not able to bleed off pressure." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Re-checked line-up. Ok. Investigated problem. Made manrider permit and checked manual IBOP. Found manual IBOP to be in closed position. Opened manual IBOP and performed line-up check by applying 15 bar. Ok." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Filled riser with SW using cmt unit. Performed pressure test of PR against RTTS plug/10 3/4' x 13 3/8' annulus to 20/203 bar for 5/10 min. Test OK, 2.1 bar drop/10 min on high pressure test and levelling off trend. 1230 ltrs pumped and 1180 ltrs bled back. Bled off pressure while maintaining overpull on riser." "On 2009-02-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Drained landing string using needle valve. Pulled hot stab out of TBC ROV panel A and inserted into TBC ROV panel B. Sat TBC ROV panel B in 'upper piston flush' 1-x-x and flushed with corrosion inhibitor. Sat TBC ROV panel B in 'parking position' and installed dummy stab. Released and retrieved 10 MT moonpool tugger to surface. Meanwhile prepared tensioner system in WH module." "On 2009-02-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued retrieving 10 MT moonpool tugger to surface." "On 2009-02-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.8 hours. Operational details: Installed centralizers, boat collision stool and tensioner ring in WH module. Meanwhile lowered PR cutting equipment down to tensioner deck. Retrieved RLGF using crane and landed on main deck. MU lifting clamp on surface riser. Pressure tested kill and standpipe manifold to 30/345 bar for 5/10 min." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Removed and POOH with handling slings from surface riser. RU scaffolding in moonpool to be able to MU NT2 connector on BOP. Meanwhile changed out saver sub on TDS and continued with house keeping." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Moved BOP to well centre and MU NT2 connector. Installed BOP tension cylinders. Meanwhile continued to chang out saver sub on TDS, repaired spinners on iron roughneck and LO PR RT with cut riser section." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared to run diverter. Meanwhile trouble shot tension cylinder failure on F-15." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box talk before running overshot and diverter. Removed outer ring and master bushings. Ran overshot. Moved BOP into well centre to re-align with diverter. NU diverter. Installed outer ring and master bushings. Removed long slings and installed BX elevator and rotating adaptor." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Filled riser with SW using cmt unit. MU, inspected seals and greased surface test plug. RIH with test plug and landed in suface WH at 20.5 m." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.8 hours. Operational details: Attempted to pressure test all connection between multibowl and BOP to 35 bar/5 min. No go. Opened lower pipe ram and closed middle pipe ram. Re-tested. No go. Re-sat test plug. No go, due to test plug was leaking. POOH with test plug. No damage seen on test plug. MU, RIH and landed back-up test plug. Filled pipe with SW. Attempted to pressure test all connections between multibowl and BOP to 35 bar/5 min. No go, due to test plug was leaking. Meanwhile RD broken tension cylinder on F-15." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: PU TDS and re-landed test plug. Applied 3 mT of block weight down on plug. Pressure tested all connections between multibowl and BOP to 35 bar/345 bar for 5/10 min. Had 2 bar (0.6%) drop in 10 min." "On 2009-02-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Function tested BOP rams. Opened BOP ram and POOH with test plug strapping the length to be 20.515 m down to landing point in surface wellhead." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.8 hours. Operational details: Flushed lines and pressure tested TIW, lower IBOP, upper IBOP and kelly hose to 35/345 bar for 5/10 min." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: MU DP stand to bowl protector RT and installed bowl protector in multibowl. POOH and RB bowl protector RT. Confirmed distance to landing point in multibowl." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: MU and RIH with Vetco 6' jetting sub from surface to below BOP. Attempted to start pumping SW through jetting tool. No go." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Found air lock in suction line to mud pumps. Bled off air from suction dampners." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Jetted SW at 4000 lpm / 48 bar while reciprocating string 3 times across BOP. RIH to 144 m with jetting sub. Jetted SW at 4000 lpm / 49 bar while reciprocating string 3 times across subsea wellhead." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH with jet sub to 150 m. Treated SW and started displacing production riser to treated SW." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH and LO jet sub from 145 m to OOH." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: RU to retrieve annulus insert in subsea WH. Removed torque dogs and fitted 2 torque pins. RIH with annulus insert RT on 5 1/2' DP from surface to 139 m. Tagged insert with 3 mT. Engaged 'J' slot and unscrewed annulus insert with 2500 Nm and 6 turns. PU free of subsea WH and attached steel tape to DP. Strapped out of hole to verify landing point in subsea WH (139.935 m). Removed annuslus insert and LO RT. Meanwhile started to change hydraulic tension cylinders on F-15 on centralizer deck." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: MU and RIH with bowl protector RT from surface to 21 m. Engaged in bowl protector and pulled protector free. POOH and LO bowl protector and RT." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: MU spear assembly as per Red Baron instructions and RB in derrick. MU adjustment sub according to Dril-Quip instructions and RB in derrick." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Removed 5 1/2' handling equipment and cleared and tidied rig floor." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RU 10 3/4' handling equipment for 10 3/4' tie-back. Stopped operation due to exhaust fumes on drill floor." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued RU 10 3/4' handling equipment for 10 3/4' tie-back. Found loose fitting on aft PRS during inspection." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired loose fitting on PRS hose. Stopped operation due to exhaust fumes on drill floor." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Continued to repaire loose fitting on PRS hose. Observed new leak while testing PRS." "On 2009-02-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Identified bursted hose on upper arm on aft PRS. Installed new hose as a temporary solution on upper arm (hose will be replaced during scheduled PRS overhault). Meanwhile continued to change hydraulic tension cylinders on F-15 on centralizer deck." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued RU 10 3/4' handling equipment for 10 3/4' tie-back." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk prior to RIH with 10 3/4' casing. PU 10 3/4' tie-back adapter and sat in slips. Observed major hydraulic leak from TDS." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Found damaged port for hydraulic hose in TDS rotating head. Isolated port and switched to redundant hydraulic line." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 11.5 hours. Operational details: Continued trouble shooting hydraulic leak in TDS rotating head. LO 10 3/4' tie-back csg onto HTS, removed PS21's, bails and elevator to have acess to TDS. Meanwhile continued changing hydraulic tension cylinders on F-15 on centralizer deck. Performed housekeeping and maintenance." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Replaced seal in rotating head and rebuilt same. Tested and observed no leaks. Continued rebuilding rotating head components." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: De-isolated drawworks and TDS. Function tested TDS and pressured up system. Tidied and cleaned oil from TDS and rig floor." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RU and function tested handling equipment for 10 3/4' csg." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 14m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH with 10 3/4' casing. PU 10 3/4' tie-back adapter and sat in slips." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: PU and RIH with 10 3/4' csg 13%Cr80 Vam Top from 14 m to 119 m." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PU 10 3/4' surface csg hanger assembly with adjustment sub and handling tool. Released casing hanger RT with 10 right hand turns and LD same." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Drained 13 5/8' surface riser through B-annulus valve on multibowl to sea. Meanwhile changed to 5 1/2' handling equipment." "On 2009-02-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: MU pre-made stand with 10 3/4' spear from derrick." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Stabbed spear into 10 3/4' casing hanger and took overpull to confirm that grapple was engaged. Landed stop plate on top of csg hanger. RIH with 10 3/4' surface casing hanger from 119 m to 136 m. RIH weight was 82 mT. Tagged subsea tie-back WH. RIH and tagged top of tie-back threads in subsea csg hanger at 139.8 m. Sat down 1 mT. Observed white painted ring through multibowl valve. Turned 6 1/2 turn clocwise to max torque at 13000 Nm. Observed red/green painted ring through multibowl valve. Took 30 mT overpull to check pre-tension in csg. Released spear. POOH and RB spear in derrick." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: PU and RIH to 28 m with pre-made 5 1/2' DP stand with adjustment sub setting tool. Locked adjustment sub ring inside 10 3/4' csg and confirmed with taking overpull. Rotated 4 turns clockwise to engage torque slots in adjusting sleeve. No go - had engaged the wrong profile. Released tool, bled off pressure and pulled up 7 cm. Increased pressure to 140 bar and pulled up another 7 cm. Locked adjustment sub ring inside 10 3/4' csg and confirmed with taking overpull. Rotated 13.5 turns clockwise to engage torque slots in adjusting sleeve. Vetco observed casing hanger movement through A-annulus valve on multibowl. Surface tie-back hanger landed out and torque increased to 9000 Nm. Released locking ring. POOH and RB adjustment sub setting tool string." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed to 10 3/4' casing handling equipment." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: MU and RIH with csg hanger RT on 10 3/4' casing landing string from surface to 20 m. MU swedge, lo-torque and cmt hose to landing string." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Lined up and leak tested the cmt line to rig floor 345 bar/5 min. Bled off pressure and lined up and leak tested the 10 3/4' surface tie-back casing against the RTTS at 319 m to 345 bar/10 min with SW. Test OK, dropped 0.8 bar (0.2%). Volume pumped 345 ltrs and had 320 ltrs in returns." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Broke out cmt hose. Released and POOH with csg hanger RT from 21 m to OOH. PU, BO and LO landing string joint with attched swedge." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RD 10 3/4' casing handling equipment and cleared rig floor." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RU 5 1/2' handling equipment." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: LO adjustment sub assembly and spear assembly. Cleared rig floor off excess equipment." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held tool box talk and picked up and RIH with 10 3/4' MS-T seal assy RT. Landed out on 10 3/4' casing hanger. Locked RT into riser. Set seal assy by applying 4300 psi to setting function. Tested seal assy trough test port in multibowl to 345 bar/10 min. Ok." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released RT from Casing Hanger and POOH with RT. Laid out same." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Held tool box talk and picked up and RIH Bowl protector and landed off in surface wellhead. POOH and LO RT." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 315m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box talk. PU and MU RTTS pulling tool. Started RIH from surface to 318 m. Tagged plug with 4 mT. PU 3 m with RTTS RT to 315 m." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 315m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Emptied trip tanks and displaced choke and kill lines to 1.25 sg mud. Displaced well with 21 m3 1.25 sg OBM at 1500 lpm." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 315m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Took up/down weight 81/78 mT. Tagged RTTS plug, screwed into the RTTS with 21 turns. Pressure dropped with 3 bars when equalizing. Flow checked well and confirmed well static. Picked up 28 mT overpull and released the RTTS plug. Well swabbed slightly when plug was pulled free. Flow checked well until it was static." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held tool box talk and POOH wet with RTTS plug from 315 m to OOH. LO RTTS plug, RT and XO." "On 2009-02-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk and changed handling equipment back to 5 1/2' DP." "On 2009-02-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH and LO one stand of 5 1/2' HWDP from derrick. Continued to LO 12 joints of 5 1/2' HWDP from below RTTS assembly. MU and RB 3 stands of HWDP for dedicated landing string in derrick. Cleaned and cleared drill floor." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: PU and MU 8 1/2' BHA and RIH from surface to 42 m." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Held tool box talk prior to handling radioactive sources. Loaded radioactive source into Ecoscope." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued to MU and RIH with 8 1/2' BHA and RIH from 42 m to 55 m." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Re-arranged 8 1/2' DC in fingerboard to acess 5' HWDP and 6 3/4' jars." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued to MU and RIH with 8 1/2' BHA and RIH from 55 m to 150 m." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Installed and tested PS-21 automatic slips." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 639m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 150 m to 639 m. Tripping speed 391 m/hrs. Meanwhile investigated VFD fault on drawworks." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 639m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Tested that 7' swage FH was compatible with 5 1/2' Vam Eis. Ok. Installed drift sub and XO. Change slips inserts to 5 1/2'." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 639m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Installed XO on string and MU to TDS. Broke circulation and pumped 2000 lpm / 120 bar. Filled pipe and performed shallow test of MWD tools." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 641m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Performed choke drill with both crews. Serviced TDS." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2816m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 641 m to 2816 m. Filled pipe every 15 stands. Tripping speed 669 m/hrs." "On 2009-02-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2920m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Broke circulation and washed down 8 1/2' BHA from 2818 m to 2881.8 m. Tagged cmt with 5 MT at 2881.8 m. Drilling parameters : 2000 lpm / SPP 168 bar / 30 RPM / torque 18-21 kNm. Up weight 175 mT / Down weight 136 mT / Rotational weight 152 mT. Continued report on F-99 for change of tension cylinders." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled out shoe track from 2881.8 m to 2914 m whilst bleeding in 1.60 sg OBM to weigh up from 1.25 sg to 1.32 sg OBM. Drilling parameters : 2000 lpm / SPP 156-200 bar / 50 RPM / torque 17-22 kNm / WOB 5-10 mT / ECD 1.40 EMW / ROP 1-20 m/hrs / Effective ROP 5.6 m/hr." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2923m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled out 9 5/8' casing shoe from 2914m to 2920m and 3 meter new formation to 2923m. Drilling parameters: Flow 2000 lpm / SPP 159 bars / String RPM 70 TQ 26-29 kNm / WOB 5-6 / ECD 1.42 EMW / MUD weight 1.32 SG / ROP 5 m/hours. Cleaned out rat hole, observed packing off, reamed at reduced weight. Verified no restrictions." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2923m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Took SCR @ shoe, ran back & tagged TD @ 2923m." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2923m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Pumped 5 m³ LCM pill and placed at TD 2923m." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: POOH from 2923m to 2817m." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Rigged up and performed FIT. Applied 51 bars equivalent to 1.50 SG. ESD from MWD 1.516 SG." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Good FIT test, rigged down hose and pump-in sub." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Flushed choke and kill lines with 1.32sg OBM." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2923m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Washed in hole from 2817m to 2923 mt. Down linked tools and set same." "On 2009-02-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3058m. The activity was categorized as 'drilling -- drill' and lasted for 10.2 hours. Operational details: Drilled 8½' hole from 2923m to 3058m. Drilling parameters: Flow 2000-2400 lpm / SPP 156-218 bars / String RPM 160 TQ 26-31 kNm / WOB 7-9 / ECD 1.44 EMW / MUD weight 1.32 SG / ROP 15-30 m/hour. Took survey after every connection." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3163m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 8½' hole from 3058m to 3163m. Drilling parameters: Flow 2400 lpm / SPP 215-218 bars / String RPM 160 TQ 25-28 kNm / WOB 6-8 / ECD 1.44-1.45 EMW / MUD weight 1.32 SG / ROP 15-30 m/hour. Took survey after every connection." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3176m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued drilling 8½' hole from 3163m to 3176m. Drilling parameters: Flow 2400 lpm / SPP 220 bars / String RPM 160 TQ 26-31 kNm / WOB 5-8 / ECD 1.44-1.45 EMW / MUD weight 1.32 SG / ROP 20-30 m/hour." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3176m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Performed sticky test. Took pressure points: MD probe TVD Reservoir press. Mud hydrostatic Pres. gradient 3141m 2958.8m 313.2 bars 412.0 bars 1.081 SG 3134m 2952.4m 312.6 bars 411.8 bars 1.081 SG 3129m 2947.7m 312.2 bars 411.2 bars 1.081 SG 3127m 2945.9m 312.0 bars 411.1 bars 1.080 SG Rig shut down." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3176m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Rig shut down due to general alarm, black out, Monitor well on trip tank. Well secure. Re- set drill floor equipment. Rotated the string at low 10rpm." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Continued drilling 8½' hole from 3176m to 3220m. Drilling parameters: Flow 2400 lpm / SPP 221 bars / String RPM 160 TQ 29-32 kNm / WOB 5 / ECD 1.45 EMW / MUD weight 1.32 SG / ROP 20 m/hour. Circulated hole clean prior to perform pressure points." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3220m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Performed sticky test at 3212m. Took pressure points: MD probe TVD Reservoir press. Mud hydrostatic Pres. gradient 3160m 2976.4m 315.5 bars 417.4 bars 1.081 SG 3156m 2972.7m 314.6 bars 417.0 bars 1.082 SG 3152m 2969.0m 314.0 bars 417.8 bars 1.080 SG 3149m 2966.3m 313.8 bars 417.7 bars 1.079 SG" "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3232m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued drilling 8½' hole from 3220m to 3232m. Drilling parameters: Flow 2400 lpm / SPP 221 bars / String RPM 160 TQ 29-32 kNm / WOB 5 / ECD 1.45 EMW / MUD weight 1.32 SG / ROP 20 m/hour." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3230m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Pulled up and circulated hole clean reciprocating the string. 2000 lpm and 161 bars." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3231m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Recorded torque and up/down/rotation weights at 3231m. 20 rpm 164 MT, 18-21 kNm. Up/down weight 194/145 MT." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3231m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Dropped 2-7/8'' drift and pumped down same at 2000lpm." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3231m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well - Well static" "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2898m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: POOH wet from 3232m to 2898m inside 9-5/8' shoe with 8½' BHA at 10m/std logging." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2898m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Recorded torque and up/down/rotation weights at 2898m. 10 rpm 151 MT, 13-15 kNm. 20rpm 155 MT 12-16 kNm. Up/down weight 177/140 MT." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2898m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well - Well static. Simultaneously serviced TDS and aft PRS." "On 2009-02-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2898m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Function tested BOP. Continued to service TDS and PRS." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2898m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pumped 5 m³ slug 1.61 SG. Investigated electrical wires on Aft PRS" "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 680m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Continued to POOH with 8½' BHA from 2898m to 680m. Pulling speed 682 m/hour. Performed kick drill: 60 sec responce time." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 680m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well - Well static." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 680m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Removed 2-3/4' drift, LO drift sub. Changed handling gear from 5½'' to 5''." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 146m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued to POOH with 8½' BHA from 680m to 146m. Pulling speed 712 m/hour." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Commenced laying out the 8½' BHA." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Continued laying out the 8½' BHA. Including radio active sources." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor. Function tested BOP shear ram." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Held tool box talk and rigged up surface handling equipment for running 7' liner. Simultaneously laid out 5½' HWDP on cantilever, drifted and measured same." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk and picked up shoe and performed integrity of float with SW." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up float joint and attempted to MU first connection. Problems with Weatherford tong stabbing guide alignment and remote control system. Laid out float and shoe due to damaged threads." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Picked up back up shoe and performed integrity of float with SW. Continued RIH with 7' liner, installed radio active market at collar 140m. Filled every 5'th jnts." "On 2009-02-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 375m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Continued RIH with 7' liner from 140m to 375m. Filled every 5'th jnts." "On 2009-02-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 411m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued RIH with 7' liner from 375m to 411m. Filled every 5'th jnt." "On 2009-02-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 411m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed out to 5½' DP elevator. Picked up Weatherford 7' liner hanger and made up same." "On 2009-02-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 425m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to change out Weatherford slips to PS21 slips." "On 2009-02-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 425m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Removed Weatherford slips from rotary, inserted PS21 slips." "On 2009-02-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 425m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with Weatherford 7' liner hanger. Removed protection pads and checked screws, filled 7' liner hanger with water. Set hanger in slips. Liner weight - 16.5 MT." "On 2009-02-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 425m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rigged down Weatherford casing tong." "On 2009-02-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 573m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH from 425m to 573m with Weatherford 7' liner hanger on 5½' HWDP picked up from cantilever." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued POOH with 7' liner hanger RT from 2766m to 2131m. Pulling speed 635 m/hour." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 5m³ 1.60 SG slug." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed kick drill: 60 sec. Cleared and cleaned rig floor prior to slip & cut drill line. Meanwhile removed ps-21 slips and installed master bushings." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held tool box prior to slip and cut drill line." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Commenced slip & cut drill line as per procedure." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Continued slip and cut. De-isolated draw works & calibrate block, activated crown-o-matic, set @ 55mt." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2131m. The activity was categorized as 'interruption -- maintain' and lasted for 2.8 hours. Operational details: Held tool box talk and repaired junction block gland on upper aft PRS. De-isolated TDS, draw works, PRS." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Held tool box talk and installed PS21 slips. Continued to POOH from 2131m to 135m. Laid out pup joint. Pulling speed 614m/hour." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk and removed PS21 slips and installed master bushing." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued to pull HWDP from 135m to 13.5m. Laid out 2 x joints HWDP & hanger running tool." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleared and cleaned rig floor." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk and laid out 7' liner hanger RT." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up cement head to break out pup jt. Laid out cement head and pup jt." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to run Jet sub for cleaning the BOP." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Held tool box talk and made up Jet sub. RIH and washed the BOP. Function the BOP and washed again. POOH and laid out Jet sub." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held tool box talk and changed inserts in elevators to 3½' DP." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 13m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked up and made up cleanout assy#1 and #2 and RIH from rotary to 13m." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 13m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed dies inserts for 3½' in iron rough neck." "On 2009-02-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 36m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Picked up 3½' DP from cantilever and RIH in singles from 13m to 36m." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 53m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Continued picking up 3½' DP from cantilever and RIH in singles from 36m to 53m." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 53m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Installed automatic slips." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 80m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued picking up 3½' DP from cantilever and RIH in singles from 53m to 80m." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 80m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed to backup elevators due to problems with primary elevators." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 371m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Continued picking up 3½' DP from cantilever and RIH in singles from 80m to 371m" "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 371m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed inserts in elevators to 5' DP." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 395m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked up and made up assy #3, 7' polish mill and well commisioner. Changed inserts in PS21. Picked up and made up assy#4, well patroler/sweep magnet." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1399m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Continued RIH well clean out assy on 5' DP from 395m to 1399m." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1399m. The activity was categorized as 'completion -- stimulate' and lasted for 0.2 hours. Operational details: Made up 5½' XO. Made up TDS and broke circulation 1000l/m 54bar." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1413m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Stopped circulation and disconnected from TDS. Broke out and laid out 5½' XO. Changed inserts in elevator to 5½''. Picked up 10-3/4' casing clean out assy and made up same." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1413m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held tool box prior to RIH with clean out assy's. Inspected PRS dies." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1413m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Problem with BX elevator function investigated. Installed gauges on elevators & tested same." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1910m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Picked up one single and continued RIH with clean up assy's from 1413m to 1910m. Made up TDS & staged up pump rate to 1800 lpm, 160 bars, reciprocated full std and scraped FLX Packer setting depth area 3 times. Up/down weight 125/110 MT." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2798m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: Continued to RIH from 1910m to 2798m. Up/down weight 160/128 MT (rpm 20 = 8-11 torque). Circulated 50m³ OBM at 1774 lpm, 162 bars." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3159m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: RIH slowly trough 7' liner top with 6' bit, while circulating with 500lpm, 24 bars and rotating (20-40 RPM), no obstruction. Continued RIH 2 stands below TOL from 2798m to 3159m, and stopped pumping." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Made up TDS. RIH until 9-5/8' scraper at 2790m, and scraped packer setting depth +/- 15m from 2790m 3 times. Down/up weight 132/164 MT, 1800 lpm, 188bar, rpm 20, 9 - 11 kNm. RIH and tagged top of liner 2812.9m, bit depth 3190.6m." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3185m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: POOH until PBR polish mill 5 m above top of 7' liner PBR. Established rotation 40 rpm and 500 lpm. Entered the PBR while rotating with the Polish Mill assy. Set down 1-2 MT on top of the PBR, while rotating, and dressed top of PBR. Pulled out of the PBR with rotation. Repeated operation 1 time without setting weight down, polished inside PBR. Pulled polish mill above liner top." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3185m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated and conditioned mud with 2220 lpm, 273 bars, 40 rpm, 10 - 12 kNm." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk and set the pack-off on well commisioner as per SPS instructions." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up on trip tank, closed upper rams, pressured up well commissioner to 70 bar/ 10 min using the cement unit." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Bled off pressure, opened upper rams, unseated the well commissioner and prepared for in-flow test of 7' liner." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Lined up for pumping base oil." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to displace DP to base oil down to TOL and perform inflow test of 7' liner." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced Kill and Choke hoses to base oil at 1000lpm." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Lined up and displaced DP to base oil 30,7m³, 0.82 SG, 500lpm, final pressure 141bars." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Allowed for thermal expansion, lined up to cement unit for pressure reading and bleeding off." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Took up/down weights 157/127 MT. Set the Well Commissioner by landing on the liner top." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Allowed for pressure to stabilize 164bar. Emptied trip tank and monitor well on flow line visually." "On 2009-02-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Bled down standpipe from 164bar in 25-30bar increments to 10bars and allowed thermal expansion. Simultaneously prepared pits and fluids for wash train." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued allowed thermal expansion. Bled down to 10bars 4 times. Final inflow test 30min/10.41 up to 12.18 bars, last 10min/0.48bar. Total volume bled off - 750liters. Simultaneously prepared pits and fluids for wash train." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3191m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pressured up DP to app. 164 bar to equalized pressure across the Well Commissioner with the cement unit- 475liters." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and unset the well commissioner 157 MT. Allowed elements to relax. Isolated down to cement unit, bled off pressure on cmt line. Picked up to 3181.5m with, with 15rpm, up weight 146 MT, neutral weight 141 MT. Polish mill 2 m above top of liner." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Continued preparing pits and fluids for wash train." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held tool box prior to commence well clean out, with all involved personnel." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Continued to prepare pits and fluids. Lined up and prepared for displacement. Meanwhile continued injecting slop, and clean cantilever & shaker area." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Started displacement of washing train. Reciprocating the sting, 40 rpm, 2000 lpm and 130bars. 10 m3 Dope Cleaner pill - 0.87 SG and 30 m³ Hi-vis push pill - 1.34 SG. Unable to continue rotation due to high torque, 20 kNm. Increased flow rate to 2500 lpm, 80 bars and started to pump batch of 15 m³ Hi-vis Soap pill - 1.02 SG." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.5 hours. Operational details: Continued to pump and displace cleaning pills out of well pumping seawater at 3000 lpm, 216 bars. Last NTU reading 505." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Held tool box talk and flushed cmt line, confirmed line up. Pressure tested well to 345 bar, Pup off vent on Mud pump liner, isolated liner and re-test to 345bars.Vetco observing B- annulus for press build up, pumped 1920l bled back same." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flow checked well - well static." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1426m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: POOH with clean out assy. from 3180m to 1426m. Pulling speed 540m/hour. Reduced tripping speed untill bit out of liner." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1413m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Laid out one single 5½'' DP, assy #5 from 1426m to 1413m." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1401m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed to 5'' handling equipment, pick up one 5'' single." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 395m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued POOH with clean out assy's on 5' DP, from 1401m to 395m. Pulling speed 1006 m/hour." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 371m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Laid out #3 and #4 clean out assy's." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Changed to 3½'' handling equipment. Held tool box talk and POOH with 3½' DP from 395m to 43m, in single on cantilever. Pulling speed 108m/hour." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed out handling equipment." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 14m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continued laying out 3½' DP from 43m -14m, in single on cantilever." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Laid out #1 and #2 clean out assy's." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to wash and clean BOP for leak testing same." "On 2009-02-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Started to pick/make up well protector, BOP clean out assembly and wear bushing running tool." "On 2009-02-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Continued make up well protector, BOP clean out assembly and wear bushing running tool." "On 2009-02-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: RIH, jetted WH area/wear bushing. RIH to 20m and engaged wear bushing. Pulled wear bushing to surface and laid out wear bushing and running tool." "On 2009-02-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Spaced out jetting sub below BOP. Removed master bushings and outer ring." "On 2009-02-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned top of diverter and diverter housing." "On 2009-02-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Jet well head, riser and BOP's with S/W. 3000 lpm, 46bars, 10 rpm." "On 2009-02-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Re-installed outer ring and master bushing. Function BOP rams and annular." "On 2009-02-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box talk and started pumping soap pill through stand pipe, choke/kill line and manifold." "On 2009-02-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 7.8 hours. Operational details: Prepared for running completion: Prepared casing tong and control unit. Made up jnt # 258 THG landing string. Waited for services personnel to arrive, delayed due to fog yesterday. Meanwhile cleaned shaker beds and pits. Prepared to install flow line on F-15." "On 2009-02-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Held tool box talk prior to RIH with 7' completion string." "On 2009-02-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 97m. The activity was categorized as 'completion -- completion string' and lasted for 4.2 hours. Operational details: Picked up and RIH with Mule shoe, seal stem, Packer SB-3, PBR and DHPG/Chemical Injection sub." "On 2009-02-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 97m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Terminated cable to DHPG according to Well Dynamic procedure. Function checked and pressure tested gauge to 10000 psi / 15 minutes." "On 2009-02-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: RIH with 7' tubing from 97m to 103m. Connected chemical injection line according to Well Dynamic procedure and installed protector clamps." "On 2009-02-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: RIH with 7' tubing from 103m to 119m. Monitored well on trip tank." "On 2009-02-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 322m. The activity was categorized as 'completion -- completion string' and lasted for 5.5 hours. Operational details: RIH with 7' tubing, Laid out joint # 7. Continued RIH with 7' tubing from 119m to 322m . Tested DHPG every 30 min. Running speed 37m/hour. Last 3 hours 60m/hour." "On 2009-02-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 920m. The activity was categorized as 'completion -- completion string' and lasted for 13.0 hours. Operational details: Continued RIH with 7' tubing, from 322m to 920m. Rejected 5 joints due to bad torque up at shoulder/damaged threads. Running speed 46 m/hour. Tested DHPG every 30 min. Total rejected 7 joints." "On 2009-02-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 981m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Continued RIH with 7' tubing, from 920m to 981m. Washed pin and box ends and re-doped threads. Found variation in pin ends surface. Investigated batch and found batch has been mixed with Åsgaard, Sleipner and Volve. The pin ends of Volve batch nice smooth threads compared to the Åsgaard/Sleipner pin ends as if they have been sand blasted and giving a rough surface." "On 2009-02-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1041m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Continued RIH with 7' tubing, from 981m to 1041m. Cleaned every pin/box and re-doped. Ran only tubing from Volve batch. Rejected 5 jnts. Total laid out 12 jnts. Running speed 24 m/hour.Tested DHPG every 30 min." "On 2009-02-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1206m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: Continued RIH with 7' tubing, from 1041m - 1206m. Ran only tubing from Volve batch. Rejected 3 jnts. Total laid out 15 jnts. Running speed 28 m/hour. Tested DHPG every 30 min." "On 2009-02-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1217m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Laid out one jnt picked new one RIH from 1206m to 1217m." "On 2009-02-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1237m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: Held tool box talk and picked up and made up GLV, installed Flatpack in guard rail on GLV." "On 2009-02-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1616m. The activity was categorized as 'completion -- completion string' and lasted for 9.0 hours. Operational details: Continued RIH with 7' tubing, from 1237m to 1616m. Rejected 3 joints. Total rejected 18 jnts. Running speed 42 m/hour. Tested DHPG every 30 min. Changed grease to OCR 325 AG API modifirer" "On 2009-02-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1808m. The activity was categorized as 'completion -- completion string' and lasted for 4.0 hours. Operational details: Continued RIH with 7' tubing, from 1616m to 1808m. Running speed 48 m/hour. Tested DHPG every 30 min." "On 2009-02-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1796m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Attempted to make up TBG. Due to bad torque up at shoulder/damaged threads as bracking out, damaged box of joint in RT. Rejected 2 joints. Total rejected 20 jnts." "On 2009-02-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1784m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Damaged 2 boxs when braking the joint above. Rejected 2 joints. Total rejected 22 jnts." "On 2009-02-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1998m. The activity was categorized as 'completion -- completion string' and lasted for 5.0 hours. Operational details: Continued RIH with 7' tubing, from 1784m to 1998m. Running speed 43 m/hour. Tested DHPG every 30 min." "On 2009-02-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2306m. The activity was categorized as 'completion -- completion string' and lasted for 5.8 hours. Operational details: Continued RIH with 7' tubing, from 1998m to 2306m. Rejected 1 joint. Total rejected 23 jnts. Running speed 53 m/hour. Tested DHPG every 30 min." "On 2009-02-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2306m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Held tool box talk made up ASV and one 7' tubing joint above." "On 2009-02-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- completion string' and lasted for 7.0 hours. Operational details: Spliced electrical and chemical injection lines below ASV. Flushed through and confirmed lines. Blanked redundant line and secured in clamp." "On 2009-02-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Ran ASV through rotary table. Rigged up ASV control line sheave. Connected blue control line above ASV. Secured lines." "On 2009-02-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Pressure tested ASV to 570bars and spare control line to 345bars for 10 minutes." "On 2009-02-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Connected electrical and chemical injection line from above ASV to reel. Pressure tested connection to 690bars / 10 minutes. Adjusted ASV control line pressure to 420bars keeping the ASV valve open. Parallel activity: Laid out 56 joints of 7' 29# 13%CrS110 on aft SB bay and measured. Started rigging up the flow line for F-15A at the WH." "On 2009-02-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Performed gauge electrical test. Challenge to get a proper test due to rain and wind. Parallel activity: Continued rigging up the flow line for F-15A at the WH. And laid out remaining joints of 7' 29# 13%CrS110 on aft SB bay and measured." "On 2009-02-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2317m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Performed electrical splice pressure test 690bars 15 min. RIH and set in slips." "On 2009-02-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2346m. The activity was categorized as 'completion -- completion string' and lasted for 4.0 hours. Operational details: Picked up and made up DHSV and connected C/L-line and leak tested same to 570 bars 10min. Inspected lines on ASV." "On 2009-02-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2804m. The activity was categorized as 'completion -- completion string' and lasted for 12.2 hours. Operational details: Held tool box talk and continued RIH with 7' tubing from 2346m to 2804m. Washed pin and box, inspected threads. Greased up pin/box prior to make up. Laid out 3 joints and changed 2 collars Total rejected 26 joints. Running speed 38m/hour. Tested DHPG every 30 min." "On 2009-02-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2804m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Picked up and made up space out string to TDS." "On 2009-02-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Verified line up applying 5 bars behind closed IBOP. Opened IBOP broke circulation 160lpm 5 bars. RIH with string. Stopped circulation as pressure built up to 6 bars. Continued RIH and set down 4 MT on no-go ring at 2817.1m. Applied 3 bars to the tubing to verified seal no returns." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Marked space out string. POOH with space out string and laid out same. As POOH the control lines got caught under the spider slip and bent. Lost signal to DHPG. Still enough lines to make up tubing hanger without making any splice." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Held tool box talk and removed Weatherford spider slips. Reconfigured banana sheaves. Installed master bushing. Return sheaves to original state." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Removed spider slips from rig floor." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2776m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Laid out 6m pup and 12m joint." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2794m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Picked up new 6m pup and made up same." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked and made up tubing hanger. Secured the control lines with a clamp on upper tubing coupling. Lowered the tubing hanger down to a convenient working height." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Cut the control lines 3 m above tubing hanger and started feeding the control lines through the tubing hanger. Checked signal to DHPG ok." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Continued feeding the control lines through the tubing hanger. Leak tested all penetrations/fittings simultaneously through the 1/8' test ports, as per Vetco procedure, to 35/345 bars 5/10 minutes." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box talk and installed C-plate, landed of tubing hanger. Laid out tubing hanger handling sub." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box talk and picked/made up tubing hanger running tool to communication collar. Connected ASV, chemical injection and DHSV lines to ports on running tool. Leak tested ASV and DHSV to 560bars 10 minutes." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Connected tubing hanger running tool lock/unlock lines to Vetco reel. Repeated test on ASV due to discrepancies." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Investigated problem. Found indication of communication between the ASV and DHSV chambers in the communication collar and running tool." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Disconnected control lines from running tool. Laid out primary running tool. Changed out seals on communication collar. Prepared back up running tool." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked/made up back-up tubing hanger running tool to communication collar. Connected ASV, chemical injection and DHSV lines to ports on running tool. Leak tested ASV and DHSV to 545 bars 10 mins." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Removed the 'C' plate. RIH with the tubing hanger. Drained riser prior to land tubing hanger. Landed the tubing hanger no-go shoulder in the Multi Bowl, slacked off weight. Observed no drag stinging into 7' liner. Verified correct tubing hanger land off and tubing hanger seal integrity, leak tested through port #1 and #2 on Multi Bowl to 35 bars/5 min." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made 7' Vam Top x 2' 1502 swedge to landing string and cement line." "On 2009-02-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Locked tubing hanger into WH." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Took 15MT overpull." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Tested tubing hanger seal at well head 35/345bars , 5/10mins." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Leak tested line/hose against lo-torq valve to 345bar/5min with Halliburton cement pump. Bled down to 10 bars. Applied 545 bars to ASV and DHSV. Opened lo-torq valve." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Pressured up tubing to 50 bar, checked pressure integrity, prior to setting packer. Held for 5 min. Volume pumped 181 litres. Closed DHSV and bled down pressure to 5 bars and observe red for 10 min. Bled back 50 litres." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Pressured up tubing to 60 bars and equalized over DHSV, 88 litres. Applied 545bars to control lines for DHSV." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Pressured up tubing 100 lpm to 345 bars 863 litres total 951 lifters. Packer set after 15 min. Continued with tubing test of 345 bars to a straight line of 15 min." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Bled down pressure to 280 bars, 190 litres bled back. Closed DHSV and bled down to 210 bars, 45 litres bled back. Performed inflow test of DHSV with 70 bars diff./15min." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Bled down pressure to 10 bars, 98 litres bled back. Performed inflow test of DHSV with 270 bars diff./30min." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Equalised pressure across DHSV, pressure up tubing 280 bar, 170 litres. Opened DHSV." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Bled down pressure in tubing to 100 bars and kept DHSV open. 550 litres bled back." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Held tool box talk prior to set FLX-packer. Increased tubing pressure to 110 bars. Lined for monitoring the THP on the stand pipe manifold. Isolated cement unit and bled down 10 bars THP verifying line up." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Lined up cement-unit to A-annulus, with hose connected to Multi Bowl, and tested same to 35/345bar for 5/10min against closed outer annulus valve." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Opened annulus valve and started to set FLX-packer." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Continued pressuring up A-annulus in steps accordance with BOT procedure to 330bar 10 min to test the production packer and set the FLX-packer. Pumped 1250 liters. Maintained 100 bars on tubing during pressure testing and setting of the FLX-packer, 330 bar 15 minutes." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Bled down pressure to 270 bars, 170 litres bled back. Closed ASV and bled down to 200 bars, 70 litres bled back. Performed inflow test of ASV with 70 bars diff./15min. THP 85 bars." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Bled down pressure to 10 bars, 120 litres bled back. Performed inflow test of ASV with 260 bars diff./30min. THP 77 bars." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Pressured up on ASV control line to 545 bars and isolated control line. Pressured up annulus above ASV from 10 bars to 270 bars, pumped 199 liters, and equalized ASV. Observed pressure drop in control line when equalizing ASV." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.8 hours. Operational details: Closed the outer A-section valve. Bled pressure down to 5 bars on the cement unit and inflow tested A-annulus valves to 265bars for 30 min." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Equalized pressure against closed outer A-annulus valve, to 270 bars, opened A-annulus valve and bleed back 900 liters." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2817m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held tool box talk prior to rig down surface equipment. Simultaneously bled down pressure in tubing." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Broke off swedge on top of tubing. Cut control lines. Rigged down sheaves." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Disconnected the landing string/THRT from TH by rotating 9 turns clockwise. Pulled out landing string and laid down same." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Rigged down surface completion equipment, tubing tong, control line reels etz." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on crane due to wind speed above 40 knots." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Removed equipment out from the rig floor." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Picked/made up BPV and centralizer, RIH and set BPV in tubing hanger. POOH with running tool and laid out same." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleared and cleaned rig floor." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to nipple down diverter, slick joint and BOP." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Rigged up for retrieving divertor and slick joint." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to nipple down diverter & BOP." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled diverter and installed master bushings. Stored diverter in set back area." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled slick joint and store on rig floor." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed tension cylinders from BOP." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Erected scaffolding at NT2 connector. Meanwhile rigged up dual lift assy for lower riser." "On 2009-02-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Completed rigging up scaffolding. Removed choke hose from BOP." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to move the BOP." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Released NT2 connector from lower riser." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Moved the BOP from well centre to test stump." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Rigged down scaffolding around lower riser." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to remove lower riser." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed special tool to PRS and removed outer ring and master bushings." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Hook slings into lower riser and took weight of 2MT. Released lower riser connector." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Pulled lower riser to surface. Retracted block and installed outer ring and master bushings." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Laid out lower riser joint." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Removed communication collar and unwrapped control lines as required. Started feeding control lines through dedicated ports in wellhead. Meanwhile prepared to install spool piece." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Fitted graphoil seals and started feeding control lines through dedicated ports in wellhead. Meanwhile prepared to install Spacer Spool." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed dart by hand in BPV in TH." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed VG137 seal ring on top of Multi Bowl and VG 63 seal ring on top on the Tubing Hanger. Filled void with oil. Lowered the Spacer Spool down from the rig floor. Installed Spacer Spool on Wellhead. Made up the locking dogs and the actuation screws." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Energized BT seal with plastic according to Vetco procedure, pressured up to 5000 psi, stabilized pressure, bled off to 500 psi." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Tested the tubing hanger void, grafoil seals and BT seals 35 bars 5 min and 345 bars 15 min. Checked communication to the Well Dynamic DHPG." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Completed control line termination on WH. Installed chemical injection line, DHSV and ASV control line exit blocks." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk and rigged up primary and back up lift lines to XMT. Lowered XMT down to Weather deck hatches." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed two hatches and support beam." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Fine tuned XMT lifting gear. Lowered the XMT and land off on spacer spool." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Installed Grey lock clamps and torqued up." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Retrieved lifting gear back to rig floor. Removed XMT lift cap with tugger." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed hatch and support beam." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Pressure tested BOT control line exit blocks for DHSV and ASV to 570bars 15 min. Parallel activity: Prepared to change calliper brakes on AFT PRS Continued with house keeping." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Well Dynamics installed DHPG line exit block. Terminated the gauge cable in the well head. Pressure tested the gauge exit block connection to 345 bars 10 min. Rigged up to install flow line spool and flow line at WH. Parallel activity: Continued to prepared to change out calliper brakes on PRS." "On 2009-02-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Continued rigging and installation of flow line spool and flow line at WH. Parallel activity: Started changing out calliper brakes on AFT PRS. Pressure tested WL BOP's on stump 345 bars 10 min." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Continued rigging and installation of flow line spool and flow line at WH. Parallel activity: Pressure tested WL BOP's on stump 345 bars 10 min. Continued changing out calliper brakes on AFT PRS. Calibrated load/tension sell for 7/16' WL cable." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Continued installation of flow line at WH. Parallel activity: Continued changing out calliper brakes on AFT PRS. Prepared WL equipment to go in the Moon Pool. Removed the big hatch for the Moon Pool." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Continued rigging and install flow line spool and flow line at WH. Parallel activity: Continued changing out calliper brakes on AFT PRS" "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued installation of flow line at WH. Parallel activity: Held TOFS (Time out for safety) with crew in relation to dropped object." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Supported and stabilized XMT due to installation of flow line. Removed blind hub from flow line. Parallel activity: Spotted wire line BOP's and other equipment in Moon pool." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Installed flow line hose on to flow line spool. Made up same. Parallel activity: Continued spotting wire line equipment in Moon pool." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed blind hub KWV and connected 5k hose. Lined up to pressure test XMT." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk/operations meeting." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Hook up control line remote controlled panel. Flushed through lines from cement unit to XMT." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed line test against KWV. 35/345 bars 5/10 min. Opened KWV and pressure tested the XMT + test of VG63 ring from the inside against dart in BPV 35/345 bars/ 5/10 min." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Bled off pressure and perform inflow test against swab and PWV 35/220 bars 5/10 min." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk with production personnel prior to test flow line. Parallel activity: Marked flow line support frame for modification." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Flushed through XMT to closed drain system. Unable to maintain pressure at 50 bars, continued pumping at 15-33 lpm to maintain pressure. Performed low pressure test 10 minutes. Increased pressure to 115bars maintaining 20-33 lpm 10 min." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Bled off and closed PWV. Run tugger down to tree and pull tree cap." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held TOFS (Time out for safety) with crew in relation to dropped object." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box talk and pulled dart and BPV. Installed tree cap." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Positioned flow line support frame for F15A below F10 hatch. Prepared to lift hatch F10 and removed flow line support frame for modification." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held tool box talk and removed F10 hatch and lifted/transferred flow line support frame from WH to heavy tool store for modification. Simultaneously held tool box talk prior to inflow test MMV, HMV and TWV." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: BOT & Vetco instrumentation connected line to XMT. Verified correct line up from cement unit with 10 bars against TWV." "On 2009-02-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lowered Well Dynamic chemical pump down to weather deck." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Vetco instrumentation installed instrumentation for chemical injection at well head. Connected Well Dynamic chemical pump, flushed lines to chemical inlet at well head." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Opened KWV flushed lines through tree cap. Closed Swab valve and open vent valve on flow line. Opened HMV pressured up the well to 220 bars 660 litres. Equalized and opened the DHSV. Closed MMV and bled pressure down to 185 bars - 35 bars LP inflow tested MMV for 10 min. Continued to bleed pressure down to 5 bars - 215 bars HP inflow tested for 10 min. Equalized pressure to 220 bars and opened MMV. Simultaneously pressured up chemical inj. line to 345 bars to test outlet block. Observed pressure. Pressure dropped to 270 bars. Pressured up chemical line to 345 bars and pressure dropped to 270 bars. Check valve in chemical sub set to 50 bars differential. Disk sheared premature to expected setting. Good indication of check valve settings." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Closed HMV and bled pressure down to 185 bars - 35 bars LP inflow tested HMV for 10 min. Continued to bleed pressure down to 5 bars - 215 bars HP inflow tested for 10 min. Equalized pressure to 220 bars and open HMV." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Closed KWV and bled pressure down to 185 bars - 35 bars LP inflow tested KWV for 10 min. Continued to bleed pressure down to 5 bars - 215 bars HP inflow tested for 10 min. Equalized pressure to 220 bars and open KWV. Bled down well to zero 660 litres back." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Close DHSV, HMV and KWV." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior rig up WL and good communiction with Vetco instrumentation." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Installed lower riser to XMT using dual lift arrangement and installed cap." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held tool box talk prior to making up chiksan manifold at XMT." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Started making up chiksan manifold at XMT." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Made up chiksan manifold at XMT and secured same." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lined up from cement unit to XMT. Flushed through to test cap on riser with 100% MEG." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to leak test Lo-torq manifold." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Connected WL test pump to test cap." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: Leak tested lo-torq manifold with WL test pump to 30/200 bars 5/10 min. Had to change out 2 Lo-torq valves. Prepared for running riser through RT." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Attempted to leak test LTV2. Greased LTV2, no go. Changed out LTV2." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Vetco instrumentation continued commissioning XMT. Parallel activity: Held tool box talk prior to rig up WL BOP's. Installed WL BOP's on riser. Dual lift. Picked up and made up riser and lower through RT and made up to BOP's. Dual lift Made up in-situ sub to riser and test cap. Opened SV with 44 turns. Flushed riser to 100% MEG." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Leak tested of riser/WL BOP's up to rig floor. 30/200bars 5/10mins. Leak tested LTV2 and CV. 30/200bars 5/10mins." "On 2009-03-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Continued commissioning XMT. Parallel activity: Continued with drop object list for derrick. Lowered flow line support frame down to the well head. Held tool box talk and spotted WL equipment on the rig floor." "On 2009-03-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Continued commissioning XMT. Parallel activity: Picked up lubricator grease injection head and made up same. Filled lubricator with 100% MEG." "On 2009-03-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Leak tested lubricator and grease injection head 30/200bars 5/10mins." "On 2009-03-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Continued commissioning XMT. Parallel activity: Continued with drop object list for derrick. Installed flow line support frame on XMT. Connected up hydraulic hose to WL BOP's Nippled up NT2 connector on BOP to stump. General maintenance on rig floor. Completed WL rig up." "On 2009-03-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Commissioned XMT. Meanwhile : -Performed housekeeping and cleaning in drilling areas -Changed wires and guards on monkeyboard tuggers -Checked and greased drillfloor equipment" "On 2009-03-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 18.0 hours. Operational details: Commissioned XMT. Progress in commissioning delayed by faulty hook up of transmitters, el hook up not according to EX requirements, configuration of transmitter ranges (lack of correct tool) and wrong labeling in wellhead junction box. Meanwhile : -Performed houskeeping and cleaning in drilling areas -Removed liners on mudpump#2 and checked studs -Opened and cleaned skimmer tank -Replaced handrails in derrick -Performed maintenance of drilling subs -Closed punch items from DROPS list and Synergi" "On 2009-03-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Commissioned XMT. Finished hook-up and testing of electrical and hydraulic utilities at 03:00. Meanwhile : -Performed housekeeping and cleaning in drilling areas -Tidied moonpool -Performed general PM in drilling areas" "On 2009-03-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 17.0 hours. Operational details: Commissioned XMT. Meanwhile perfomed PMs in drilling areas." "On 2009-03-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Checked valve status on XMT. Checked isolation tags and certificate issued by production department." "On 2009-03-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held toolbox talk for WL operation." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Hooked up hoses for local control to HMV and DHSV. Switched valve on HMV to local control. Opened valve on DHSV exit block. Opened HMV and lined up to pump from cement unit. Applied 520 bar to DHSV control line. Pumped MEG from cement unit and equalised across DHSV with 50 bar. Volume pumped 110 liter." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Bled off pressure on well though closed drain system. Meanwhile held toolbox talk for gun handling. Had TOFS due to unclear competence requirements for running tugger winches." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Made up PGGT-D correlation tool to cable head. Tested tools according to Schlumberger procedure. De-isolated HTS." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Ran HTS to drillfloor. Picked up 1st 4,5' 20 ft gun section with tugger and guided to well centre. Hung off guns in WL riser. Picked up 2nd 4,5' 20 ft gun section and made up same using C-spanner and chain tongs. Re-arranged lower WL sheave due to conflict with lubricator. Armed firing head. Picked up PGGT-D and firing head and made up same to guns. Ran in with guns and tagged SV at 17 m MD." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Stabbed on WL lubricator and made up quick union. Hooked up hose to in-situ test sub. Tested connection to 30/200 bar 5/10 min - ok. Opened KVW. Opened SV partly. Topped up lubricator with 200 liter of MEG. Closed KWV and LTV2. Opened HMV. Opened SV fully. Set depths on Seawell and Schulumberger counters." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 440m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH with 4,5' guns on 7/16' EWL from 17 m to 440 m MD. Took up/down weights 1800/1300 lbs. Powered up Shlumberger logging unit." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3155m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: RIH with 4,5' perforating guns on 7/16' EWL from 440 m to 3155 m MD. Ran carefully thorugh DHSVat 478 m MD and verifed open by upwards pass. Up down weights below simulations. m MD Up (kg) Down (kg) 1000 1180 1020 2000 1430 1280 3000 1610 1443" "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3148m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Correleated perforation guns using GR/CCL and reference log." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3148m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval 3148 m to 3135,5 m MD." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 225m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: POOH with 4,5' perforating guns from 3148 m to 225 m MD. Powered down logging unit and barriered off wellbay." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: POOH with 4,5' perforating guns from 225 m MD to surface." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Closed SV with 42 turns. Recorded SIWHP 26,8 bar. Closed HMV. Bled down pressure to 5 bar. Inflow tested HMV and recorded XMT pressure gauge in PCR - ok." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Opened SV/KWV and and bled off pressure in lubricator to closed drain. Closed SV/KWV." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk for laying out perforating guns." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Disconnected quick union on WL riser. Hoisted out WL BHA. Hung off guns on C-plate, broke and laid down guns. Confirmed 100% detonation." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Cut 7/16' EWL. Built new cabel head." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk for handling perforation guns." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Made 2 ea 20 ft 4,5' guns sections using C-plate, C-spanner and chaing tong." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Armed firing head. Made up CCL/firing head to perforation guns." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Stabbed and lubricator and made up quick union. Set depth on Schlumberger and Seawell counters." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Hooked up test hose to in-situ sub. Tested connection to 30/200 bar 5/10 min - ok. Opened SV partly. Open KWV and topped up lubricator pumping MEG from cement unit. Equalised pressure across HMV with 28 bar. Closed KWV, opened HMV and SV." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 215m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH with 4,5' guns on EWL from 17 m to 215 m MD. Powered up logging unit. Removed barriers in wellbay. m MD Up (kg) Down (kg) 1000 1034 921 2000 1258 993 3000 1353 953" "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3115m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: RIH with 4,5' perforating guns on 7/16' EWL from 215 m to 3115 m MD. Ran carefully through DHSV at 478 m MD." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3115m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Correlated guns using CCL and reference log. Adjusted depth as required." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3136m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval 3123 m to 3135,5 m MD. Good indication on current and cable tension. Observed small flicker on SIWHP." "On 2009-03-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 600m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: POOH with 4,5' perforating guns on 7/16' EWL from 3135 m to 600 m MD." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: POOH with 4,5' perforating guns on 7/16' EWL from 600 m MD to surface. Powered down logging unit at 215 m MD. Barriered off wellbay. Pulled WL BHA into toolcatcher. Closed SV and verified toolstring above SV. Recorded SIWHP 37,5 bar. Closed HMV. Opened SV partly." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Opened KVW and bled down pressure in XMT cross to 5 bar. Inflow tested HMV to 32 bar differential pressure for 10 min. Monitored and recorded pressure in PCR. No pressure increase in XMT cross recorded, pressure stable at 4,6 bar - ok." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Hooked up Nitrogen hose to WL riser needle valve. Purged riser with Nitrogen and bled off pressure to closed drain. Bled down pressure in WL riser/lubricatro to zero. Closed SV and TKV." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held toolbox talk for laying out WL BHA and rig down WL equipment. Cleaned drillfloor due to hydraulic fluid spills." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Broke quick connector and lifted off WL lubricator. Broke out gun sections using C-plate and chain tongs. Laid out guns and firing head/CCL. Confirmed 100% detonation. Rigged down lubricator and laid down on HTS. Cut WL. Rigged down WL sheaves. Installed lift cap on WL riser and slung up with braided slings (dual lift). Installed elevator around coupling on WL riser (primay lift)." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Broke WL riser quick union on XMT. LIfted riser ~1 m above XMT. Installed treecap." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Lined up to pump from cement unit. Pressured up to 30 bar against treecap. Pressure increased 8 bar in 15 min and levelled out at 38,5 bar (assumed SIWHP) - not able to seat HMV at low differential. Pressured up to 200 bar. Observed 0,25 bar/min drop - ok." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Bled off pressure to closed drain to 40 bar after test of treecap. Flushed 200 liter MEG from cement unit to closed drain due to potential HCs in cement line, isolated cement unit on LTV2. Bled off pressure to zero to closed drain." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Closed MMV. Closed SV. Opened needle valve on treecap. Pressure tested SV to 40/200 bar 5/10 min pumping MEG from cement unit - ok, recorded test in PCR. No visual leaks observed on needle valve. Bled off pressure to zero to closed drain. Closed treecap needle valve." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting for inflow test of DHSV." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Flushed lines from pit to cement unit for pumping brine. Lined up to pump down well from cement unit." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Equalized across HMV with 40 bar. Opened HMV. Recorded SIWHP 49,2 bar." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Bullheaded 3 m3 MEG followed by 6,6 m3 1,03 brine and 1,2 m3 MEG. Pumprate 100 lpm / 45-55 bar. Closed DHSV from local control panel." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Bled off pressure above DHSV from 45 bar to 5 bar to closed drain." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Inflow tested DSHV to 40 bar differental for 30 min. Recorded test in PCR. Pressure increased from 5,1 bar to 5,8 bar - ok." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Equalised across DHSV with 33,5 bar. Closed HMV and bled off pressure above to 5 bar to closed drain." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Inflow tested HMV - ok." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Open KVW. Equalized across HMV with 35 bar and opened same. Bled off pressure above DHSV to zero to closed drain. Closed HMV and DHSV." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Rigged down valve manifold on KWV. Hooked up Seawell test pump to treecap." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Pressure tested KWV 30/200 bar 5/10 min with Seawell test pump - ok. Charted test in PCR." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Installed cap on KWV. Opened KWV. Pressure tested KWV cap to 30/200 bar 5/10 min -ok. Recorded test in PCR." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Unhooked Seawell test pump hose, closed needle valve on treecap. Removed hoses for local control panel. Hooked up permanent hydraulic control hoses to HMV and DHSV exit block. Shifted handle on HMV to quick dump. Cleaned XMT." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Hooked up line from cement unit to A-annulus. Performed line test - ok. Deisolated permanent hydraulic controls to XMT. Applied opening pressure on ASV line." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Pumped in A-annulus and equlized ASV with 60 bar. Bled of pressure to zero. Matching pumped and bled back volumes (210 l), i.e. ASV opened." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Closed A-annulus valves, unhooked cement hose and installed blind flange" "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk for re-arranging hatches on Weather deck." "On 2009-03-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Re-arranged hatches on Weather deck. Handed well over to production. **** End of operations ****" "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to skidding operation." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.2 hours. Operational details: Skidded cantilever package from F-1 slot to F-15 slot. Observed hydraulic oil leak on starboard forward skid unit." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Removed leaking hose from skidding unit, installed new hose and pressure tested same. Meanwhile installed 1502 flange on F-15 KWV and rigged up surface manifold, re-routed test hoses." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Skidded rig over F-15 slot." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Re-installed cantilever stairwell. Meanwhile conducted TBT prior to rigging up wireline equipment & handling hatches." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Removed permanent hatch on F-15 slot. Removed tree cap." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Lowered wireline riser and checked rig alignment." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Skidded rig forward to align with F-15 well center." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Installed split hatches on F-15 slot." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Installed hose from cement unit to kill wing valve." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Landed wireline riser on tree." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Placed barriers and performed TBT for line testing using cement unit." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Tested line to KWV with cement unit with 20/345 bar for 5/10 min. Good test." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Opened KWV and SV. Filled riser with packer fluid. Pressure tested rig-up to 20 bar, unable to get a good low pressure test." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Connected AWS test pump to riser cap and pressure tested against SV with 30/345 bar for 5/10 min." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for bullheading operation." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Opened MMV and HMV, 19 bar pressure in tree cross. Applied 520 bar control line pressure on DHSV. Lined up for pumping SW with rig pumps. Applied 25 bar pressure behind KWV." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Discovered gauge on Xmas tree only rated to 100 bar. Closed HMV, bled pressure in tree cross and installed gauge with proper pressure rating." "On 2013-10-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Opened HMV and KWV. Staged up pumps and equalized over DHSV (70bar). Commenced bullheading operation pumping SW with 1200 lpm/70 - 67 bar." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Bullheaded well with SW, 1200 lpm 67-112 bar. Pumped in total 188 m3 of seawater. SPP after bullheading SW 33 bar. Observed ~100 bar pressure in wireline riser, indicating SV leaking from below." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Lined up to pump 1,21 sg OBM kill mud. Staged up pumps and pumped mud with 1200 lpm/ 127 - 96 bar. Pressure increased to 195 - 199 bar when OBM entered perforations. Pumped total 94 m3 kill mud (1,5x well volume). Bled pressure to zero. Monitored WHP. Well dead. Closed in well with HMV and KWV." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Rigged up surface lines on tree and 10 3/4' x 7' annulus. Tested same to 30/345 bar for 5/10 min." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Hold TBT. Picked up lubricator from HTS." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting with day shift prior to picking up toolstring." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Removed riser cap. M/U 5,75' drift toolstring for run #1 on slickline. Stabbed lubricator and M/U same. Leak tested lubricator/QTS to 30/200 bar for 5/10 min." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Opened well as per well entry procedure. RIH w/ run #1 (5,75' drift) from surface to top of DHSV at 477 m. Applied 520 bar to open DHSV. Not able to run through." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Evaluated situation and discussed way forward." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Rigged up line from cement unit test line to KWV routed via choke manifold. Meanwhile AWS pressured up WHP to 127 bar and ran through DHSV. Not able to pull up through DHSV." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Pressure tested line to 30/200 bar for 5/10 min." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation. Meanwhile investigated DHSV control line on Xmas tree. Vetco changed out C77 block w/ needle valve for DHSV control line on Xmas tree. C77 block plugged." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Opened DHSV, POOH with drift run to above Xmas tree. Opened KWV. Commenced bleeding down WHP from 130 - 95 bar to trip tank. Stopped bleed down due to low H2S alarm in trip tank." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: TOFS. Evaluated situation and added scavenger to treat fluid in trip tank." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Bled down WHP f/ 95bar to zero. Total volume bled back 1,56 m3." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: RIH w/ run #1 5,75' OD drift from surface to 3070 m taking returns via KWV and choke to t/t. Observed resistance while passing ASV and DHG." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: POOH w/ drift run from 3070 m to surface." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Pulled tool into catcher, lined up to leak test XMT cross to 70 bar with cement unit." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Leak tested Xmas tree to 70 bar. Lined up and displaced OBM from riser to trip tank using nitrogen." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Broke out lubricator, cleaned and L/O toolstring. L/O lubricator to HTS." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Changed grease injection head and sheaves from S/L to 5/16' e-line. Re-arranged wireline skid. Installed and calibrated SLB depth counter." "On 2013-10-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: P/U lubricator and M/U same. Lined up to test rig-up via KWV and tree. Tested lubricator and W/L riser to 30/200 bar for 5/10 min." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Broke out lubricator. P/U and M/U toolstring for run #2 (EVO plug). Stabbed lubricator and M/U QTS. Leak tested QTS to 200 bar 10 min. Opened SV and HMV." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 5.2 hours. Operational details: RIH w/ run #2 (EVO) 5,72' OD plug from surface to 3030 m. Worked toolstring through ASV (FLX-4) at 495 m." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Correlated BHA across interval 3000 - 3070 m. Set plug at 3049 m." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: POOH from 3049 m to above the Xmas tree." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Closed HMV and SV. Pulled toolstring into catcher. Leak tested across Xmas tree to 70 bar for 10 min. Flushed wireline riser and lubricator with nitrogen. Broke out lubricator. L/D toolstring." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Pressured tested EVO plug to 20/240 bar for 5/10 min. Pumped and bled back 932 l." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: R/D lubricator. Re-configured AWS winch. Hooked up add-on drum with 7-46 SLB cable. Calibrated weight cell and installed depth counter. Meanwhile isolated rigfloor equipment. Changed out oil on TDS. Cleared pipe deck to L/O 3 1/2' DP. Installed new cladding on drag chain." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Installed AWS pump in sub on W/L riser, connected hose for returns to trip tank. SLB built rope socket/cable head and prepared tools on deck for W/L run #3 USIT/CBL." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Interrupted preparation due to lifting on cantilever. L/O 40 joints 3 1/2' DP." "On 2013-10-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: SLB prepared primary and backup tools on deck for W/L run #3 USIT/CBL." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: SLB tested primary and backup tools on deck. Calibrated depth sensors. Installed sheaves. Meanwhile performed weekly maintenance on fwd and aft PRS. Installed new cladding on drag chain. Cleaned and tieded rig floor." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for M/U toolstring and USIT/CBL run." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: M/U BHA for run #3 (USIT/CBL). Zeroed tool and checked toolstring at surface. Opened SV and HMV." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: RIH w/ run #3 from surface to 3039 m." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Logged USIT/CBL across interval 3040 - 2742 m. Performed two repeat passes across same interval." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Waited on confirmation from town on log data quality." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: POOH from 2742 m to surface. Average pulling speed 20 m/min." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Closed HMV and SV. Broke and L/D run #3 USIT/CBL toolstring." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.2 hours. Operational details: R/D SLB add-on cable from AWS unit. Reconfigured AWS winch to run 5/16' e-line. R/D pump-in sub with return hose." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: M/U weight bars to cable head, stabbed lubricator and M/U same. Lined up to test riser and lubricator." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Tested lubricator and W/L riser to 20/200 bar for 5/10 min using the cement unit." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Flushed riser and lubricator with nitrogen back to trip tank." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: SLB prepared toolstring on rig floor. Rerouted lines to multibowl, lined up to test same." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: P/U and M/U BHA for run #4 (tubing punch). Tested annular line-up to 20/200 bar for 5/10 min. Pressured up annulus to 5 bar." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: M/U lubricator and tested QTS to 200 bar for 10 min. Filled riser with cement unit via KWV." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Opened HMV and SV. RIH w/ run #4 (tubing punch) from surface to 250 m. Lifted barriers and powered up SLB unit." "On 2013-10-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: RIH w/ run #4 from 250 m to 2840 m." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Bled of lubricator pressure from 34 bar to 2 bar via closed drain. Closed KWV. Verified ASV open on AWS local control panel." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Performed correlation pass across interval 2840 - 2700 m. Performed tie-in pass on same interval. Positioned puncher with top shot at 2782 m. WHP 0 bar/ Annulus pressure 3 bar. Punched interval 2782 - 2785 m. Observed annulus pressure 28 bar." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: POOH w/ run#4 from 2782 m to 250 m." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made PA announcement and placed barriers. Powered down SLB unit." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: POOH from 250 m into tool catcher. Closed HMV and SV." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Broke lubricator. L/D toolstring on deck. All guns fired." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Verified line-up for circulating tubing and annulus. Opened HMV and KWV. Staged up pumps and pumped 1,21 sg OBM with 1000 lpm/ 20 bar to FCP 100 bar. Pumped 65 m3." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: R/U slick line for run#5 (DHSV lock open sleeve)." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: P/U and M/U BHA for run #5 (Lock open)." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Removed hose from multibowl and hooked up same to KWV. Bled off 20 bar to t/t." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Opened SV and HMV. RIH w/ run #5 (lock open) to DHSV at 477 m." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Set lock open ring as per procedure." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Jarred up and sheared pin between D probe and lock mandrel." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: POOH from 477 m to surface. L/D running tool and stinger assembly." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH w/ GS/M pulling tool from surface to 477 m." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Jarred up to release the lock and retrieve FLO from well, no success." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.2 hours. Operational details: Jarred down to release GS/M pulling tool." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH from 477 m to surface. FLO left in hole." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Held TBT with nightshift. Re-configured toolstring, including hydraulic jar and TDR." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: RIH w/ jarring toolstring and engaged FLO at 477 m." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Jarred upwards on FLO. Observed free after 15 hits. Confirmed 300 lbs additional weight." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: POOH from 477 m to 284 m w/ 35 m/min. Observed loss of tension and weight. Stopped POOH." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for way ahead and handling loose wire safely." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH from 284 m to surface. Toolstring parted at time delayed release below cable head." "On 2013-10-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Prepared fishing BHA to fish parted toolstring." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: M/U fishing BHA w/ overshoot and bell guide, re-dressed core and tested same." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: RIH with fishing BHA to 470 m." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Engaged fish at 470 m, confirmed additional weight. POOH with 30 m/min from 470 m to surface." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: L/D recovered toolstring, FLO left in hole. M/U assembly to fish FLO." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: RIH with FLO fishing assembly to 477 m." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Engaged FLO, confirmed additional weight. POOH from 477 m to surface." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Closed SV. L/D fishing BHA and FLO on deck." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: M/U toolstring run #6 (shallow EVO plug). RIH on S/L and positioned EVO plug at 35 m. Set plug using DPU w/ timer (40 min). POOH with toolstring #6 and L/D same." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Lined up and P/T shallow plug to 20/240 bar for 5/10 min. Good test. Meanwhile layed down lubricator." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.2 hours. Operational details: Pulled wireline riser and L/O same. Removed W/L BOP and spool. Cleared all W/L equipment from rig floor." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Removed hatches on slot F-15 above Xmas tree. Opened tree and drained remaining OBM using samson unit." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed flow line elbow from tree. Meanwhile informed production department and requested to shut in wells as per SIMOPS procedure." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: R/U and pulled fox hole. Rigged up lifting equipment on tree. Held TBT prior to lifting of Xmas tree." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Lifted Xmas tree into moon pool. Lifted spool piece to rig floor." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Landed Xmas tree on transport frame. Installed master bushings and lowered fox hole." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: GE Vetco removed control lines from multibowl. Meanwhile lifted surface riser joint to rotary. L/O 3 1/2' DP, prepared finger board for 3 1/2' DP stands. Changed out fox hole and IRN dies, adjusted PDM to 3 1/2' DP." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lowered communication collar onto multibowl. GE Vetco installed same. Held TBT for handling hatches and riser joint." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed cross beam and hatches in moon pool." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed master bushing. Ran surface riser and M/U same to multibowl." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed half moons and prepared BOP for skidding." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Moved BOP to well centre." "On 2013-10-11, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed slick joint. Installed Master bushings. Meanwhile R/U diverter and prepared for skidding." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Prepared for skidding the cantilever aft. Held TBT for skidding operation." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Skidded rig 13 cm aft to align BOP over riser." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Soft landed BOP on surface riser. Installed diverter. Notified production department that production can commence." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Errected skaffold for access to NT-2 connector." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: M/U NT-2 connector. Meanwhile rigged down handling chains, installed elevators and rigged up for running S/L." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Installed BOP tensioning system. Meanwhile filled surface riser and BOP with 1,21 sg OBM. Cleaned and cleared rigfloor Held TBT for pressure testing. Lined up for pressure testing BOP connection." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested BOP connector against shallow set plug and blind shear ram with 20/345 bar for 5/10 min." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: M/U toolstring to retrieve shallow EVO plug." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: RIH and latched onto plug at 35 m. Equalized pressure, released plug and let elements retract for 30 min. POOH to surface." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: R/D wireline equipment." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: R/U for picking up cutting BHA #1 and 3 1/2' DP." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for upcoming operation with all parties involved." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: M/U cutting BHA #1 and X/O. M/U assembly to TDS." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Tested cutting tool at surface, cutters open at 300 lpm and 6 bar." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 85m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: P/U singles while RIH w/ cutting BHA #1 on 3 1/2' DP from surface to 85 m." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 85m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Fitting burst on IRN. Isolated and repaired same." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: P/U singles while RIH on 3 1/2' DP from 85 m to 474 m. Avg. tripping speed 195 m/hr." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Callibrated block positions with Baker sensors." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Positioned string and cut 7' tubing above DHSV at 474 m with 400 lpm, 29 bar, 100 rpm, 2-5 kNm. Good indications on surface." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Rig blacked out." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Recovered from blackout. Re-started TDS and mud pumps. Unable to start drawworks lube oil pumps, troubleshot w/ electrician. Maintenance department troubleshot rig power failure. Held TBT for picking up 3 1/2' DP with night shift." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Checked cut distance with 400 lpm / 28 bar. 0,5 m cut." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Attempted to pass cut, no go. Rotated string at 120 rpm to relax knives. Stopped rotation and passed through cut." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Broke out TDS and l/o X-over." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 765m. The activity was categorized as 'workover -- other' and lasted for 2.2 hours. Operational details: P/U singles while RIH w/ cutting BHA #1 on 3 1/2' DP from 474 m to 765 m. Avg. tripping speed 128 m/hr." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 765m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: P/U X-over and made up TDS." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 761m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Broke circ. 600 lpm / 65 bar, 500 lpm/ 56 bar. Took parameters, up 84 t, down 79 t. Positioned cutter at 761 m. Cut casing w/ 400 lpm, 46 bar, 100 rpm. Good indications on surface." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 761m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed flow check. Well static." "On 2013-10-12, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 761m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: L/O X-over and 3 1/2' DP single." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 761m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for POOH and racking 3 1/2' DP w/ fwd PRS." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.0 hours. Operational details: POOH w/ cutting BHA #1 on 3 1/2' DP from 761 m to surface, pulled wet. Avg. tripping speed 277 m/hr." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Inspected cutting BHA and L/O same. B/O x-over." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Changed handling equipment." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for rigging up csg equipment." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged up 7' tubing equipment." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U tubing hanger running tool. M/U tool to x-over and to TDS." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH to 20,5 m. Engaged into TH as per Vetco procedure. Picked up to 18,5 t, confirmed string free." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Flow checked, well stable." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting with day shift prior to pulling completion." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled THRT, reset drawwork limits due to stand height. Landed TH in c-plate." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Broke THRT from hanger and removed same with PRS." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed communication collar. Performed check for radiation, non measured." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: R/U air lines for cable drum and impact wrenches. Function tested same." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Placed handling tool on HTS, P/U and checked same. M/U and P/U tubing hanger, removed c-plate and installed auto slips." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cut control lines, broke TH and pup below. L/O assy to deck." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 5.0 hours. Operational details: POOH 7' tubing including control lines from 450 m to surface. Removed clamps and spooled 4 ea control lines to reel while POOH. Performed radiation spot checks on every 10th joint. Zero readings." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Cleaned and taped up cut on last joint. L/O same to deck." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT prior to rigging down casing equipment." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: R/D casing tong and associated equipment. Changed elevators to 5 1/2' DP." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: RIH with retrieval tool and pup joint. B/O and L/O same." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Changed to 3 1/2' handling equipment. R/U auto slips." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: P/U two singles from deck. M/U same and installed X-over. Parked stand in aft PRS." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: P/U and M/U cutting BHA #2 (FLX-4) from RKB to 25 m. Installed x-over." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Surface tested cutting assy with 600 lpm / 6 bar." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT with night shift for RIH and cutting FLX-4." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 461m. The activity was categorized as 'workover -- other' and lasted for 2.2 hours. Operational details: RIH w/ cutting BHA #2 on 3 1/2' DP from 25 m to 461 m." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 461m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: P/U double with aft PRS. M/U TDS." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 461m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: B/O 3 1/2' DP connection and filled pipe." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 499m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: RIH with BHA. Hung up at 499,3 m, 5 t down weight. Attempted to pass restriction. Turned pipe and set down weight. No sucess. Checked space out. Depth corresponding with 7' tubing cut at 473,8 + 0,5 m. Rotated with 14 kNm. String stalled out. Pulled up with 37 t overpull and broke free." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 472m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: POOH above cut at 473,8. Worked area with taper mill, 80 rpm." "On 2013-10-13, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 499m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Ran back in hole. Observed stop sub entering cut at 498,6 m. Tagged obstruction at 499,3 m. Worked string with 5 t down and attempted to pass obstruction. No success. Evaluated situation and decided to POOH." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 499m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: B/O TDS and performed TBT for POOH and racking 3 1/2' DP stands." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 345m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: POOH w/ FLX cutting BHA on 3 1/2' DP from 499 m to 345 m. Pulled wet." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 345m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Troubleshot pipe grip on aft PRS. Switched to fwd PRS." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 28m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: POOH on 3 1/2' DP from 345 m to 28 m. Experienced problems racking stands in foldable fingerboard with fwd PRS." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 28m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Removed slips and bowls." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 28m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Pulled cutting BHA above rotary and inspected NoGo ring and cutter. No mark indications, knives closed and taped." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for laying out of BHA." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Cleaned rigfloor after wet trip prior handling BHA." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: L/D FLX cutting BHA." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Cleared rigfloor and changed handling equipment." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Prepared drift run with 5,75' taper mill. P/U spear assembly with taper mill. Meanwhile discussed way forward with onshore organization." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT with day shift, discussed TOFS and MOC." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: B/O taper mill and L/D spear assembly." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Changed handling equipment from 5 1/2' to 3 1/2'. M/U 5 3/4' taper mill to 3 1/2' DP." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 462m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: RIH w/ drift BHA on 3 1/2' DP from surface to 462 m." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: M/U TDS and washed from 462 m to 474 m w/ 1000 l/min, 43 bar." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 476m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Reamed from top 7' tubing cut at 474 m to 476 m w/ 1000 l/min, 43 bar, 50 RPM, 3-4 kNm. Made 3 passes. No obstructions." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 505m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Racked circulation stand. RIH w/ 5,75' drift BHA from 462 m to 505 m, passing through DHSV and FLX-4." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: POOH from 505 m to 0 m. Pulled wet." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rigfloor after wet trip." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Changed handling equipment from 3 1/2' to 5 1/2'." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to handling rig tongs." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.2 hours. Operational details: Re-arranged FLX cutting BHA as per Baker instructions. Measured M/U BHA #2 and double checked space out." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Surface tested cutter blocks, 200 lpm, 5 bar. RIH w/ BHA to 33 m." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Removed auto slips, installed PS 21." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 462m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: RIH w/ FLX cutting BHA #2 on 5 1/2' DP from 33 m to 462 m." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 462m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Filled string w/o screwing in to avoid premature cutter activation, 400 lpm / 3 bar." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: RIH to 499,7 m bit depth. Set down 4 t weight, unable to pass FLX (5,988' ID) with 5,75' stb. Pulled free with 6 t overpull. Attempted to rotate 5 rpm, 8 kNm. String stalled out. Pulled free w/ 10 t overpull and discussed way forward." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 33m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: POOH w/ FLX cutting BHA #2 on 5 1/2' DP from 499 m to 33 m. Pulled wet." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 33m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Removed PS 21 slips and installed master bushings." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 33m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held TBT for handling BHA." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Pulled BHA from 33 m to surface." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Inspected BHA. Observed marks on stab shoulder. Secured knives. B/O stab and re-installed same higher up in BHA. Removed master bushing and installed PS 21 slips." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: RIH w/ modified FLX cutting BHA #3 on 5 1/2' DP from 33 m to 474 m." "On 2013-10-14, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 503m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Entered top of cut at 474 m, continued to run in. Landed 8' NoGo on top of cut at 503,1 m bit depth." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 503m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Marked pipe at land off point 503,1 m. Picked up 0,98 m to position cutter at planned cut depth 500,6 m. Marked pipe. Landed string on top cut and verified space out. Filled pipe w/ 400 lpm." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 503m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Positioned string at cut depth. Cut FLX according to Baker instructions. 100 rpm, 400 - 800 lpm, 5 - 8 kNm. Observed pressure drop, increased flow to 1000 lpm and kept cutting for 5 min. Stopped rotation and set down weight. Released FLX approx. 10 cm downwards. Repeated to set down 10 t for 10 min as per Baker instructions." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 503m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Flow check, well stable." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 33m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: POOH w/ modified FLX cutting BHA #3 on 5 1/2' DP from 503 m to 33 m. Pulled wet." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 33m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Removed PS 21 slips and installed master bushings." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Pulled BHA to surface and inspected same. Removed ~2 m control line from spear assy. L/D FLX cutting BHA #3." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: P/U and M/U overshot assembly to retrieve DHSV/FLX assembly." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 451m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: RIH w/ 8 3/8' overshot on 5 1/2' DP from surface to 451 m." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: M/U TDS and took parameter, 78 t down, 81 t up. Broke circ. w/ 600 lpm, 7 bar. RIH and engaged fish with 10 rpm, 1-2 kNm. Picked string up 3 m, 5 t overpull." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 474m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Allowed FLX elements to relax for 30 min. Meanwhile flowchecked well. Well stable." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 7m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: POOH with 7' tubing, DHSV and FLX assembly on 5 1/2' DP from 474 m to 7 m." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 7m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Changed from PS21 to manual slips. Installed master bushing." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Held TBT. POOH w/ overshot BHA. Disengaged from tubing as per Baker procedure." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Allowed climbers access to derrick to complete critical work in connection with Westcon survey." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Reset grapple and L/O overshot." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: R/U handling equipment for pulling 7' tubing and DHSV/FLX assembly." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 4.0 hours. Operational details: B/O tubing cut. POOH and L/O 7' pups, DHSV/FLX assemblies and tubing below FLX. Removed clamps and spooled control lines. L/O assemblies with crane." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: R/D handling equipment. Removed control line spooling unit to deck for emptying." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 5m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: P/U and M/U overshot and bumper sub. RIH w/ same. Installed auto slips." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 733m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: RIH w/ 8 3/8' overshot on 5 1/2' DP from 5 m to 733 m. Avg. tripping speed 760 m/hr." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 761m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: M/U TDS, took parameters, up 90 t, down 85 t. RIH to 755 m and reamed over tubing cut at 761 m with 2000 lpm, 20 bar, 10 rpm, 4 kNm. Engaged tubing, 60 bar and 12 kNm torque. Picked up and pulled out of PBR. No overpull." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 732m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: POOH with 7' tubing on 5 1/2' DP from 761 m to 732 m. Set slips. Problem to get slips to hold." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 732m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Held TBT. Removed PS21 slips and installed master bushing." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.8 hours. Operational details: POOH with 7' tubing on 5 1/2' DP from 732 m to surface. Controlled speed as hole not taking correct volume." "On 2013-10-15, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Pulled overshot above rotary. Cleared control lines and set tubing string in slips. Released overshot and L/O same." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2030m. The activity was categorized as 'workover -- completion string' and lasted for 1.5 hours. Operational details: Installed handling equipment for 7' tubing. B/O 7' tubing stump and L/O same." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1996m. The activity was categorized as 'workover -- completion string' and lasted for 1.5 hours. Operational details: POOH with 7' tubing. Removed clamps and spooled control lines. L/O joints on deck. Experienced difficulties to get slips to grip." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1996m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: TOFS - Held TBT to discuss use of slips and job sequence, evaluated risks." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1705m. The activity was categorized as 'workover -- completion string' and lasted for 3.8 hours. Operational details: POOH with 7' tubing. Removed clamps and spooled control line. L/O joints on deck. Performed radiation spot checks every 10 joints." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1705m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with upcoming shift." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1312m. The activity was categorized as 'workover -- completion string' and lasted for 3.5 hours. Operational details: POOH with 7' tubing from 1705 m to 1312 m. Removed clamps and spooled control line. L/O joints on deck. Performed radiation spot checks every 10 joints." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1300m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: While L/O tubing joint, string in rotary slipped to dog collar. P/U joint and M/U to string. Set string using manual slips. L/O joint. Re-installed auto-slips." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1300m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: Auto-slips not able to grip string. Changed out manual slips onto auto frame." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 814m. The activity was categorized as 'workover -- completion string' and lasted for 3.8 hours. Operational details: POOH with 7' tubing from 1300 m to 814 m. Removed clamps and spooled control line. L/O joints on deck. Performed radiation spot checks every 10 joints." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 814m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Changed dies on Weatherford slips. Cleaned and cleared rig floor." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 778m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: POOH with 7' tubing from 814 m to 778 m." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 778m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: While L/O tubing joint, string in rotary slipped. P/U joint and M/U to string. Replaced worn dies. Re-set slips and L/O joint." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 646m. The activity was categorized as 'workover -- completion string' and lasted for 2.2 hours. Operational details: POOH with 7' tubing from 778 m to 646 m. Removed clamps and spooled control line. L/O joints on deck. Performed radiation spot checks every 10 joints." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 646m. The activity was categorized as 'workover -- completion string' and lasted for 1.5 hours. Operational details: Attempted to set slips on joint several times, no success. Removed Weatherford auto slips/dog collar assy. Removed master bushing. Installed PS30 slips." "On 2013-10-16, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 320m. The activity was categorized as 'workover -- completion string' and lasted for 3.0 hours. Operational details: POOH with 7' tubing from 646 m to 320 m. Removed clamps and spooled control line. L/O joints on deck. Performed radiation spot checks every 10 joints." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 2.5 hours. Operational details: POOH with 7' tubing from 320 m to surface. Removed clamps and cut control line. L/O joints on deck. L/O DHPG/CI sub assembly. Performed radiation spot checks every 10 joints." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 2.5 hours. Operational details: Removed PS30 slips and installed master bushing B/O 7' tubing pup from tubing hanger retrieval tool. L/O same. R/D casing handling equipment. Cleaned and cleared rigfloor." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Removed lower IBOP and saver sub from TDS." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Isolated all drill floor equipment for service and inspection. Inspected TDS, dollies and both PRS." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Repaired leak on aft PRS." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Cleared rig floor of cut control lines." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Serviced TDS, travelling block and dolly." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Serviced and inspected aft PRS." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.2 hours. Operational details: Changed dies in TDS pipe handler. Installed lower IBOP and saver sub." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 8m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: P/U and M/U the 9 5/8' Safelock plug and R/T." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 8m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS 21 slips." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1783m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: RIH w/ Safelock plug on 5 1/2' DP from 8 m to 1783 m." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1818m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: M/U TDS and RIH to 1818 m. Established circulation and washed the setting area, 1100 l/min/ 22 bar. Installed the 9 5/8' Safelock mechanical plug at 1818 m (11,5 right hand turns). Set down 20 t weight on plug. Function tested ball valve as per Archer instructions." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1818m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Lined up and leak tested the plug to 20/240 bar for 5/10 min from below. Good test." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1818m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Closed ball valve and released R/T as per Archer procedure." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: POOH on 5 1/2' DP from 1817 m to 170 m." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for displacement to SW." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: Pumped base oil and soap pills as per plan. Displaced well from 170 m to surface w/ 2400 l/min and 60 rpm." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH w/ on 5 1/2' DP from 170 m to surface. L/O Safelock running tool." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Closed shear ram and flushed across kill and choke into trip tank." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing cement plug from above." "On 2013-10-17, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Confirmed line up from cement unit. Pressure tested the Safelock plug to 20/240 bar for 5/10 min. Good test." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Held Statoil TOFS with drilling crew #3." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U Vetco MS-T retrieval tool and M/U same as per Vetco instructions. Tested tool on surface. Installed hoses and Vetco pump." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with retrieval tool and landed off at 20,4 m. Set down 2 t." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Engaged retrieval tool w/ LH turns. Locked same into riser using Vetco pump." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Pressured up tool to release MS-T seal. Attempted several times to release seal, max. 62 t overpull. Unable to pull free. Verified dogs released. Disengaged tool and pulled to surface. Checked tool and ran back in. Vetco verified max. pull on tool. Engaged tool and increased overpull in increments to 75 t. Pulled free MS-T seal." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH w/ MS-T retrieval tool, L/D same. R/D Vetco equipment." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Rigged up lines on multibowl to drain riser. P/U stand from derrick and M/U connections to max. torque. P/U Drilquip adjustable sub setting tool from deck." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT for running adjustable sub tool and releasing tension from surface tieback." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U Drilquip tool and x-over. RIH to 14 m. M/U TDS." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Latched tool into adjustable sub as per DQ instructions." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Drained riser." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Rotated string left hand and removed tension from tieback string as per DQ instructions. Max. torque 23,7 kNm." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Observed tieback string had backed off." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Attempted to release adjustable sub tool several times. No success." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Pressured up string to 140 bar to work tool pistons. M/U tieback string w/ 5 right hand turns. Attempted to release DQ tool w/o success." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT for laying out tieback hanger w/DP and Drillquip tool." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Released 10 3/4' surface tieback w/ 5 left hand turns. Pulled hanger to surface. Removed bushings and installed PS 30 slips." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Attempted to release DQ tool on surface w/o success." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/U handling equipment for 10 3/4' casing." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: L/O surface hanger, Drilquip tool and single of 5 1/2' DP." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.0 hours. Operational details: POOH with 10 3/4 60,7ppf 13Cr80 VAM Top casing from 110 m to surface. L/O joints to deck." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.0 hours. Operational details: R/D handling equipment for 10 3/4' casing and cleared rig floor." "On 2013-10-18, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Assisted hydraulic mechanic on derrick work basket Removed equipment from moonpool. Maintenance and preparation for changing wires on fwd and aft PRS. Held Statoil TOFS with deck crew #3 and third party personnel." "On 2013-10-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Performed cleaning and housekeeping in shakers and pump room. Prepared to change wire on aft manriding winch. Removed drillfloor hatch to moonpool and transfered Xmas tree to maindeck. Conducted high wind checks in derrick and drilling areas." "On 2013-10-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Cleaned and cleared cantilever. Changed out wires on fwd and aft PRS. Prepared for N/D BOP and diverter. Changed wire on aft manriding winch. Conducted high wind checks in derrick and drilling areas. Prepared moonpool for deluge test. Held TOFS with drill crew #2 and third party personnel." "On 2013-10-19, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Changed out wires on fwd and aft PRS. Cleaning and housekeeping. Maintained valves in pump room." "On 2013-10-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Changed out wires on fwd and aft PRS. Cleaning and housekeeping. Replaced contingency kill hose on manifold in moonpool (for F-12). Pressure tested hose." "On 2013-10-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Pressure tested contingency kill manifold in moonpool. Performed pull test on fwd and aft PRS. B/O and L/O damaged top single on DP stand #19, P/U and M/U single from deck. R/B stand. Greased valves on kill manifold. Function tested deluge system on drillfloor and moonpool. R/D leaking low torque valve from kill manifold. B/O and L/D 3 1/2' from derrick." "On 2013-10-20, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: B/O and L/D 3 1/2' from derrick. Repaired leaking low torque valve. Performed cleaning in pit- /pumproom. Crew members participated in e-learning courses." "On 2013-10-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: P/T contingency kill manifold in moonpool. Performed cleaning in pit- /pumproom. Performed housekeeping in drilling areas." "On 2013-10-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Weekly inspection on aft IRN. Performed high wind checks. Changed out fwd PRS wire, interrupted job due to wind speed above 45 knts. Performed cleaning and housekeeping in drilling areas." "On 2013-10-21, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Continued to change out fwd PRS wires. Performed cleaning and housekeeping in drilling areas." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Rigged up kill contingency manifold for F-12 w/ new hoses. Changed out fwd PRS wires. Greased manifolds on drill floor. Cleaned spacer pits. Performed cleaning and housekeeping in drilling areas." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile performed general rig maintenance: Calibrated fwd PRS after wire change out. Tested drilling equipment after isolations. Greased standpipe manifold. Pressure tested production riser to 20/200 bar for 5/10 min." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: P/U and M/U running tool for Archer Safelock plug. Checked tool on surface." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 205m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: RIH w/ running tool on 5 1/2' DP from surface to 205 m." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 205m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Installed PS 21 slips." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1538m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.8 hours. Operational details: Waited on weather to pull production riser. Meanwhile: RIH on 5 1/2' DP from 205 m to 1538 m. Avg. tripping speed 762 m/hr." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1538m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Displaced production riser to 1,21 sg OBM. 2000 l/min and 30 bar. Diverted SW returns to dedicated pit." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1810m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: RIH on 5 1/2' to 1810 m. Established circulation and washed area above plug w/ 2400 lpm, 40 bar." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1815m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Engaged plug as per Archer instructions. Pressured up above ball valve to 30 bar. Attempted to open ball valve w/o success. Bleed pressure to 20 bar. Opened ball valve and observed pressure drop." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1815m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Released Safelock plug w/ 15 RH turns and let packer elements relax." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1815m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: RIH below plug setting depth and confirmed plug free. Flow checked well for 15 min. Well stable." "On 2013-10-22, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1010m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.8 hours. Operational details: Waited on weather to pull production riser. Meanwhile: POOH w/ 9 5/8' Safelock plug on 5 1/2' DP from 1815 m to 1010 m. Avg. tripping speed 460 m/hr." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 8m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.8 hours. Operational details: Waited on weather to pull production riser. Meanwhile: POOH w/ 9 5/8' Safelock plug on 5 1/2' DP from 1010 m to 8 m. Avg. tripping speed 577 m/hr." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser. Meanwhile: L/D the 9 5/8' Safelock plug including RT." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Cleaned and cleared rig floor." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: Waited on weather and Weatherford casing crew - Helicopter cancelled due to fog Meanwhile prepared for running 2 7/8' cement stinger and setting P&A plugs in 7' liner." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Performed inventory on rig floor and moonpool work aloft locker. Tested BX elevators with 2 7/8' inserts and 2 7/8' tubing. Rigged up 2 7/8' auto slips and dog collar. Performed general rig maintenance. Repaired netting around cantilever handrails and logging unit deck. Climbers inspected derrick work basket and manriding winch sheave in crown." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Lifted equipment to rigfloor. R/U casing tong, power frame and control equipment and function tested same." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 420m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Picked up, made up and RIH open ended to 420 m w/ 45 joints of 2 7/8' tubing, 10 jnts/hr." "On 2013-10-23, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 420m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser. Meanwhile: Changed to 5 1/2' handling equipment. Installed x-over f/ 2 7/8' to 3 1/2' and f/ 3 1/2' to 5 1/2' DP." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 420m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: R/D handling equipment Removed bowls and installed PS 21 slips" "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2793m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 4.0 hours. Operational details: RIH w/ open ended 2 7/8' cement stinger on 5 1/2' DP from 420 m to 2793 m." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3053m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.0 hours. Operational details: Took weight @2793 m. Pulled up to 2761 m, broke circulation 1000 lpm, 81 bar. Washed in hole with 500 lpm, 40 bar from 2761 m and tagged top of plug @ 3052,6 m with 2 tons." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3053m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Made up cement head and connected surface lines." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3053m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.8 hours. Operational details: Broke circulation with 500 lpm, 45 bar, increased flow in increments to 2230 lpm, 280 bar and circulated 2 x bottoms up with 1.21 sg OBM while rotating 10 rpm. Pressure tested the surface lines to 200 bar, 5 min. OK." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3053m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Spotted P&A plug #1; pumped 8.0 m3 1.60 spacer with 800 lpm, mixed and pumped 8.24 m3 1.90 sg gas tight slurry with 640 lpm, followed by 3.8 m3 1.60 sg spacer. Displaced cement with 24.9 m3 1.21 sg OBM with 2200 lpm, 10 - 20 RPM." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 3053m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Disconnected surface lines and laid down cement head." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2600m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Pulled out of cement with 2 7/8' stinger from 3052 m to 2600 m. No back-flow observed." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2600m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Installed 2 x sponge ball. Circulated 1.5 x bottoms up with 2200 lplm, 290 bar at 50 RPM, 9 - 12 kNm. Observed traces of cement and spacer in returns.No OBM diverted to slops. Performed time-out for Statoil information meeting with crew during circulation." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2600m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped slug." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1430m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.0 hours. Operational details: POOH with 2 7/8' cement stinger on 5 1/2' DP from 2600 to 1430 m. Avg. tripping speed 290 m/hr." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1430m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed pre-job Meeting with new crew prior to POOH with 2 7/8' cement stinger on 5 1/2' DP." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1191m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH with 2 7/8' cement stinger on 5 1/2' DP from 1430 m to 1191 m. Avg. tripping speed 950 m/hr." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1191m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Performed time-out for Statoil information meeting with crew." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 830m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH with 2 7/8' cement stinger on 5 1/2' DP from 1191 m to 830 m. Avg. tripping speed 480 m/hr." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 830m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Filled trip-tank. Cleared and cleaned rig-floor." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 422m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH with 2 7/8' cement stinger on 5 1/2' DP from 830 m to 422 m. Avg. tripping speed 816 m/hr." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 422m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig-floor prior to rigging up 2 7/8' tubing handling equipment." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 422m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to rigging up 2 7/8' tubing handling equipment." "On 2013-10-24, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 422m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: R/U handling equipment and broke 5 1/2' x 3 1/2' x 2 7/8' x-over. Racked back last 5 1/2' DP stand and changed handling equipment to 2 7/8'." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 422m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: R/U casing tong, installed slips and changed handling equipment to 2 7/8'." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 422m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to lay down single joints of 2 7/8' tubing." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.8 hours. Operational details: L/D single joints of 2 7/8' tubing while POOH from 422 m to surface. Avg. tripping speed 73 m/hr." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: R/D and lifted out tubing handling equipment including casing tong." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U 8 1/2' Clean-out bit and bit-sub. Installed float." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Inspected and cleaned dies in aft PRS, changed out worn dies." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 204m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' Clean-out bit on 5 1/2' HWDP from surface to 204 m. Avg tripping speed: 408 m7hrs." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 204m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed auto slips." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2590m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 4.5 hours. Operational details: RIH with 8 1/2' Clean-out bit on 5 1/2' DP from 204 m to 2590 m. Filled pipe every 20 stands. Avg tripping speed: 530 m/hrs." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2590m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Broke circualtion 1330 lpom, 68 bar and recoreded parameters: up-/down-weight 160 / 120 tons. Free rotating weight 136 tons, 11 - 14 kNm, 25 RPM. Circulated 1500 lpm, 70 bar, 50 RPM while reciprocating string." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2627m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Washed in hole with 500 lpm, 23 bar from 2590 m to 2624 m without rotation. Took weight @ 2624 m. L/D top single and M/U next stand. R-tagged @ 2624 m with 500 lpm, 23 bar, pulled up 3 m and established drilling parametres 1500 lpm, 65 bar, 60 RPM, 13 - 16 kNm, RIH and dressed TOC from 2624 m to 2627 m. Observed resistance decreasing. Picked up 2 m, stopped rotation and reduced flow to 500 lpm, 23 bar. Continued washing in hole and observed immediate tag @ 2627 m." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2637m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Picked up 3 m to 2624 m and established drilling parameters 2000 lpm, 93 bar, 80 RPM, 14 - 18 kNm. RIH and dressed cement from 2627 m to 2630 m with 2 - 3 tons WOB. Picked off bottom and stopped rotation and reduced flwo to 300 lpm, 17 bar. Tagged TOC with 10 tons. Re-established drilling parameters 2000 lpm, 93 bar, 80 RPM, 14 -18 kNm. RIH and dressed cement from 2630 m to 2637 m with 5 tons WOB. Avg ROP 28 m/hrs." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2634m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Picked off bottom and circulated bottoms up with 2500 lpm, 126 bar, 80 RPM, 15 - 22 kNm while reciprocating string." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2637m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Stopped rotation and reduced flow to 300 lpm, 17 bar. RIH and tagged TOC with 10 tons for 2 min 2637 m." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 2610m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pumped slug. R/B stand and M/U single joint of 5 1/2' DP." "On 2013-10-25, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1900m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: POOH with 8 1/2' Clean-out bit from 2610 m to 1900 m. Avg tripping speed: 568 m/hrs." "On 2013-10-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1825m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH with 8 1/2' Clean-out bit from 1900 m to 1835 m. Engaged top-drive and broke circulation 2500 lpm, 96 bar, 80 RPM, 8 - 11 kNm. Circulated bottoms up while reciprocating string in 9 5/8' EZSVB setting area from 1825 m to 1835 m." "On 2013-10-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1817m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped slug and Filled trip-tank." "On 2013-10-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.2 hours. Operational details: POOH with 8 1/2' Clean-out bit from 1817 m to surface on 5 1/2' DP and HWDP." "On 2013-10-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Laid down 8 1/2' bit. Cleared and cleaned rig floor. Performed general rig maintenance." "On 2013-10-26, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Performed genereal rig maintenanec. Removed worn cement hose from cement manifold. ROV removed debris around template." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.5 hours. Operational details: Performed general rig maintenance. Removed worn cement hose from cement manifold. ROV removed debris around template." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: P/U and M/U the 9 5/8' EZSV with running tool." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1824m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: RIH with 9 5/8' EZSV from surface to 1824 m on 5 1/2' DP. Restricted running speed to 1.5 min/stand. Avg tripping speed: 456 m/hrs." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1834m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Broke circulation with 800 lpm, 32 bar and worked packer setting area from 1824 m to 1934 m 3 times." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1829m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Recorded up- / down- weights 125 / 108 tons. Set 9 5/8' EZSV with 40 right hand turns, sheared with 23 tons up weight and waited 2 min. Set down 9 tons on plug and waited 2 min and confirmed 9 5/8' EZSV runnig otol free by picking up 5 m. Top of packer 1828.6 m." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1824m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Pumped slug." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 600m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: POOH with 9 5/8' EZSV running tool from 1824 m to 600 m. Avg tripping speed: 816 m/hrs." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 600m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Filled trip-tank." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 205m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: POOH with 9 5/8' EZSV runing tool from 600 m to 205 m. Avg trippin gspeed: 790 m/hrs." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 170m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: Engaged top drive and positioned 9 5/8' EZSV running tool @ 170 m. Broke circulation and conditioned mud with 1500 lpm., 10 bar. Held tool box talk prior to displacement of riser from 1.21 sg OBM to seawater." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 170m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Pumped wash train of 5 m3 base oil, 5 m3 hi-vis pill and 5 m3 soap pill with 1500 lpm, 9 bar. Lined up and displaced riser to seawater with 2400 lpm, 11 bar, 60 RPM. Flushed kill line with seawater." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 5m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: POOH with 9 5/8' EZSV running tool from 205 m to 5 m. Avg trippin gspeed: 660 m/hrs." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Removed bushings and pulled 9 5/8' EZSV running tool through rotary." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Closed shear ram, lined up and pressure tested the surface lines to 195 bar for 2 min. Ok. Pressure tested the 9 5/8' EZSV from above to 20/195 bar for 5/10 min. Ok. Pumped a total of 1506 ltrs and bled back same." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Opened shear ram, removed auto slips and installed master bushing." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: L/D 9 5/8' EZSV running tool." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to nippling down BOP. Meanhile: shut down production in preparation for nippling down BOP." "On 2013-10-27, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Nippeled down diverter and rigged up for nippling down BOP. Meanwhile: shut down production in preparation for nippling down BOP. Production confirmed shut down @23:50." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Nippled down diverter and rigged up for nippling down BOP." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to nippling down BOP." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Nippled down BOP, transferred and landed same on test stump." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.2 hours. Operational details: Prepared Claxton tool, ran and connected same to high pressure surface riser joint. Drained riser through multi-bowl on lower annulus side outlet. Meanwhile: Performed DROPS check prior to pulling riser." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Nippled down side outlets on riser, leaving two bolts on each outlet." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to removing half-moons on high pressure surface riser joint." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed half-moons on high pressure surface riser joint." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled high pressure surface riser joint free." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Removed bushings, pulled out with high pressure surface riser joint and laid out same to deck." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Nippled down multi-bowle side outlets and transferred same to rig floor." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U multi-bowl running tool and RIH with same on 5 1/2' DP. Landed running tool in multi-bowl and engaged same with 5 right hand turns. Picked up 47 tons overpull." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Bled down tension cylinders, transferring weight from tensioning system to top drive." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.8 hours. Operational details: Rigged down tensioning system. Meanwhile: Installed cement hose to cement manifold and pressure tested same to 345 bar. Ok. Performed general rig maintenance." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to rigging down tensioning system with new crew." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Rigged down tensioning system." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to running guide wires and remove F10 hatch." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Removed F10 hatch and rigged up guide wires. Meanwhile: Performed Pre-job meeting on drill floor prior to splitting riser spider." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to running guide wires." "On 2013-10-28, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Ran 10 tons and 6 tons guide wires and attached same with ROV." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Ran 10 tons and 6 tons guide wires and attached same with ROV." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Set down 15 tons on tie back connector and launched hot-stab connector on guide wires. ROV removed dummy hot-stab connector. Flushed through hot stab connector and installed same with ROV." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to unlatching and pulling production riser." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pressured up hot stab connection to 3000 psi. Unlatched tieback connector and picked up riser off the wellhead. No overpull observed. Retrieved hot-stab with ROV and re-installed dummy hot-stab." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled production riser on 5 1/2' DP and set multi-bowl running tool in slips. R/B stand of 5 1/2' DP, removed bushings and pulled production riser to first connection in rotary." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to installing riser spider." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Installed riser spider in rotary. Installed hydraulic hoses and function tested spider." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Picked up riser until flange above spider and closed dogs. Landed off tension joint and disconnected flange." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to laying out production riser." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Laid down tension joint to cantilever." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Installed lifting sub on upper pup joint. Picked up upper pup joint and retracted TDS. Installed lifting sub on splash zone joint #4 (double). Laid down upper pup joint to cantilever." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Picked up splash zone joint #4 and removed fairings. Removed mussels etc. around flanges and bolts. Broke out connection, picked up and retracted TDS. Installed lifting sub on double #3 / #2. Laid down splash zone joint #4 to cantilever." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Picked up double #3 / #2 and removed fairings. Removed mussels etc. around flanges and bolts. Broke out connection, picked up and retracted TDS. Installed lifting sub on joint #1 and lower pup joint (double). Laid down double #3 / #2 to cantilever." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Released guide wires from production riser and disconnected from template using ROV. Production shut in all wells according to SIMOPS." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Picked up joint #1 and lower pop joint and removed fairings. Removed mussels etc. around flanges and bolts. Laid down joint #1 and lower pop joint to cantilever." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to picking up and run drilling riser." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Prepared Tie Back Connector / stress joint assembly on cantilever, removed lifting sub and re-slung joints. Meanwhile prepared tuggers to run guide funnel." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crew. Installed lift sub on stress joint." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Picked up TBC / stress joint assembly and ran through rotary, landed same in spider." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Function tested TBC on drill floor. Meanwhile installed guide funnel." "On 2013-10-29, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Picked up lower riser pup joint." "On 2013-10-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Picked up lower riser pup joint. Prepared seal faces on joint connection and made up same. Tested connection and ran down with riser joint." "On 2013-10-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Picked up intermediate riser joint #4. Prepared seal faces on joint connection and made up same. Tested connection and ran down with riser joint." "On 2013-10-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Peformed pre-job meeting. Removed nylon guides on tensioner deck to allow TBC to run through. Installed same again. At 04:45 hrs informed Production to start production according to SIMOPS." "On 2013-10-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Picked up intermediate riser joint #7. Prepared seal faces on joint connection and made up same. Tested connection and ran down with riser joint." "On 2013-10-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Installed fairings on HPDR connections. Double secured HPDR in elevators and riser spider. At. 09:30 hrs informed production to start up according to SIMOPS." "On 2013-10-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: Waited on weather. Meanwhile: Cleaned and tidied wellhead deck and drill floor. Performed planned maintenance. Cleaned BOP's prior to pressure test. Installed BOP test mandrel." "On 2013-10-30, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather. Meanwhile: Tested BOP's to 20 / 345 bar for 5 / 10 minutes. Performed planned maintenance and general housekeeping." "On 2013-10-31, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Tested BOP's to 20 / 345 bar for 5 / 10 minutes. Performed planned maintenance and general housekeeping." "On 2013-10-31, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Tested BOP's and manifolds to 20 / 345 bar for 5 / 10 minutes. Performed planned maintenance and general housekeeping." "On 2013-10-31, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Installed hatches on well head deck. Tested manifolds to 20 / 345 bar for 5 / 10 minutes. Performed planned maintenance and general housekeeping." "On 2013-11-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Installed hatches on well head deck. Performed planned maintenance and general housekeeping." "On 2013-11-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Performed planned maintenance and general housekeeping." "On 2013-11-01, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Removed well head deck hatches from well F-10 and F-15. Performed planned maintenance and general housekeeping." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.8 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Performed planned maintenance and general housekeeping. At 03:00 hrs informed Production to shut down according to yellow SIMOPS procedure." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to run HPDR. Meanwhile: Performed pre-job meeting prior to run HPDR." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Installed fairings on connection between intermediate joint #4 and #7. Picked up and tailed in intermediate joints #3 and #6 (double). Prepared seal faces on joint connection and made up same. Tested connection." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.2 hours. Operational details: Waited on weather prior to run through splash zone with riser. Meanwhile: Performed planned maintenance and general housekeeping. Held pre-job meeting prior to run riser through splash zone." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 79m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Ran through splash zone with HPDR from 50 m to 79 m." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Picked up and tailed in intermediate joint #4 and upper pup joint (double). Prepared seal faces on joint connection and made up same. Tested connection and ran in sea with HPDR from 79 m to 103 m." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior changing of elevators." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 103m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed to side door elevators for lifting tension joint." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 121m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Picked up and tailed in tension joint. Prepared seal faces on joint connection and made up same. Tested connection and ran in sea with HPDR from 103 to 121 m." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 121m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed side door elevators and installed 5 1/2' DP elevators." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 127m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Picked up and tailed in BOP joint with Claxton NT2 running tool. Prepared seal faces on joint connection and made up same. Tested connection. Ran BOP joint and Claxton tool through rotary." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 127m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Made up X-over and stand of 5 1/2' DP to Claxton tool handling pup. Meanwhile: ROV removed debris cap from wellhead and installed VX ring gasket." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 127m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to landing riser / TBC." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Ran in sea with HPDR from 127 m to 137 m. Entered riser guide funnel and continued running down to top of wellhead." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 137m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Released riser guide funnel and parked same on seabed." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lowered hotstab connector to seabed using 6 ton winch. ROV removed dummy hotstab and installed hotstab in TBC. Switched connector valves to run position." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Landed riser and TBC, sat down 20 Ton weight. Closed connector by applying 3000 psi, observed indicator rods shifting to closed position." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed 30 Ton overpull test on TBC, ok." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Retrieved hotstab connector and 10 Ton guide wire. Released 6 Ton guide wire and recovered same." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held pre-job meeting." "On 2013-11-02, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Installed well head deck hatches on well F-10 and F-15. Erected scaffolding around riser in moonpool. Rigged up horizontal tensioner system on HPDR in moonpool to minimize movement due to heavy sea." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Erected scaffolding around riser in moonpool." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Filled riser. Pressure tested riser to 200 bar for 10 minutes." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Installed centralizers and boat collision stool." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.8 hours. Operational details: Installed tensioning ring and cylinders. Transferred riser weight from TDS to tension cylinders. Adjusted riser tension to 150 MT Installed centralizers on upper wellhead deck." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Rigged up control hoses and released Claxton tool from riser." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Made up single to Claxton tool. Removed bushings and outer ring, pulled Claxton tool to drill floor. Installed outer ring and bushings. Laid Claxton tool out on cantilever." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Modified scaffolding in moonpool. Maenwhile: Performed pre-job meeting prior to installing slick joint and diverter." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Modified scaffolding in moonpool. Maenwhile: Prepared equipment to run diverter. Performed pre-job meeting prior to nipple up BOP. At 11:00 hrs informed production to shut down according to SIMOPS red procedure." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 5.2 hours. Operational details: Moved BOP to well centre. Landed BOP on riser and made up NT2 connector. Installed slick joint and diverter. Rigged up BOP tension system. Cleaned and cleared rigfloor and moonpool areas. At 15:00 hrs informed Maersk Production to restart production according to SIMOPS procedure." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to pick up cutting BHA." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: Picked up and made up 10 3/4'casing cutting assembly." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pressure tested BOP cennection to 20 / 200 bar - 5 / 10 minutes." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Tested cutters at surface, knives opened at 330 liter/min." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 700m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: RIH restricted with 10 3/4' casing cutting BHA on 5 1/2' DP from surface to 700 m. Average tripping speed 400 meter/hr." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 700m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Filled pipe with 220 liter/min." "On 2013-11-03, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1433m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: RIH restricted with 10 3/4' casing cutting BHA on 5 1/2' DP from 700 m to 1433 m. Average tripping speed 938 meter/hr. Observed leak hydraulic leak on PS-21 slips." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1433m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed masterbushings." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1470m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH restricted with 10 3/4' casing cutting BHA on 5 1/2' DP from 1433 m to 1470 m." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1470m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: Filled pipe with 240 liter/min." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1497m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Connected TDS and placed cutter at 1497 meter. Cut casing with 841 liter/min, 46-59 bar, 120 rpm, 5-15 kNm. Confirmed cut by setting down 5 Ton on cut off edge at 1497,5 meter." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1497m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Flow checked well, gaining 270 liter/hour. Meanwhile installed PS-21 slips." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1497m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: Circulated bottoms up with 1000 liter/hour, 34-37 bar." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1497m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flow checked well, static." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1497m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Pumped 6,7 m3 1,54 sg slug." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 788m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: POOH with 10 3/4' casing cutter on 5 1/2' DP from 1497 m to 788 m. Average tripping speed 945 meter/hr." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 788m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Filled trip tank. Held pre-job meeting with oncoming crew." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: POOH with 10 3/4' casing cutter on 5 1/2' DP from 788 m to 21 m. Average tripping speed 945 meter/hr." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed master bushings." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: POOH with 10 3/4' casing cutter on 5 1/2' DP from 21m to surface. Laid down cutting assembly to cantilever. Cleaned and cleared rigfloor." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: Picked up and made up lock down assembly retrieval tool. RIH with retrieval tool on 5 1/2' from surface to 130 m. Made up TDS and jetted area between 130 m and 142 m twice with 3000 liter/min, 54 bar. Engaged lock down assembly retrieval tool at 139 meter. Pulled lock down assembly free with 17 ton overpull. POOH with lock down assembly and laid out same." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed master bushings and installed BHA Wash Tool. Cleaned and cleared rigfloor." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1493m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.8 hours. Operational details: Picked up spear assembly from HTS. RIH with spear from surface to 129 meter. Made up TDS and recorded up / down weights 80 / 77 Ton. RIH to 138 meter. Continued to run in and engaged casing at 149 meter. Pulled casing free with 175 Ton, Pulled to 1493 meter." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1493m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to displacement." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1486m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.8 hours. Operational details: Pulled slowly OOH with casing from 1493 m to 1486 m. Established circulation with 1,25 sg mud in increments of 400 liter/min to 2200 liter/min, 94 bar. Circulated until equal MW in / out." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1486m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Flow checked well for 15 minutes, gained 360 liter/hour." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1477m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Racked back 1 stand of 5 1/2' DP to 1477 meter." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1477m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Flow checked well for 30 minutes, gained 360 liter/hour." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1477m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: Circulated bottoms up with 2435 liter/min, 96 bar, MW in / out 1,25 sg." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1477m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Flow checked well, static." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1477m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Pumped 7,5 m3 1,54 sg slug. Performed pre-job meeting prior to POOH with 10 3/4' casing." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1396m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.8 hours. Operational details: Picked up and released spear from hanger. Laid out spear assembly to cantilever. Attempted to brake out hanger, observed failure on casing tong." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1396m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Repaired faulty electrical connection on casing tong." "On 2013-11-04, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1396m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Broke out hanger and laid down same." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1396m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Rigged up flush mounted slips. Transferred HTS rollers from FWD to AFT cantilever." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1384m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: POOH with 10 3/4' casing from 1396 m to 1384 m." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1384m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Removed guide from flush mounted slips due collars hanging up." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1373m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: POOH with 10 3/4' casing from 1384 m to 1373 m. Observed gain in trip tank. Investigated volumes, well in balance." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1283m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: POOH with 10 3/4' casing from 1373 m to 1283 m. Stopped due to problems with casing tong, not able to release grip." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1283m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Repaired casing tong." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1142m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 3.0 hours. Operational details: POOH with 10 3/4' casing from 1283 m to 1142 m. Average pulling speed 5 joints/hr." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1142m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crews." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1142m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Inspected equipment prior to use." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 552m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 7.0 hours. Operational details: POOH with 10 3/4' casing from 1142 m to 552 m. Average pulling speed 8,9 joints/hr. Observed elevators out of alignment." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 552m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Replaced U-bolt on TDS bail clamp." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 207m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 4.2 hours. Operational details: POOH with 10 3/4' casing from 552 m to 207 m. Average pulling speed 8,5 joints/hr." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 207m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crews." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.8 hours. Operational details: POOH with 10 3/4' casing from 207 m to surface. Average pulling speed 9,5 joints/hr." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to rigging down handling equipment." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Rigged down handling equipment for 10 3/4' casing. Cleaned and cleared rigfloor. Broke out and laid down 10 3/4' spear." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to laying out spear assembly." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Broke out and laid down spear assembly." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to RIH with wearbushing." "On 2013-11-05, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Picked up and RIH with wearbushing and jetsub assembly." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Picked up and RIH with wearbushing and jetsub assembly. Jet washed WH with 2950 liter/min, 50 bar. Installed wearbushing. POOH with wearbushing RT and jetsub assembly, laid down same." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Picked up and made up 13 3/8' casing cutting assembly. Tested cutters at surface." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH restricted with 13 3/8' casing cutting BHA on 5 1/2' DP from surface to 107 m." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Changed from master bushings to PS-21 slips." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH restricted with 13 3/8' casing cutting BHA on 5 1/2' DP from 107 m to 350 m. Average tripping speed 486 meter/hr." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Emptied trip tanks." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1392m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: RIH restricted with 13 3/8' casing cutting BHA on 5 1/2' DP from 350 m to 1392 m. Average tripping speed 595 meter/hr." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1392m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Filled drill pipe." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1426m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Made up TDS and RIH from 1392 m to 1426 m. Recorded up / down weights, 110 / 100 Ton." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1426m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to displacement." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1426m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Cut 13 3/8' casing with 80 rpm, 5-10 kNm, 400-800 liter/min, 16-36 bar. Pressure dropped to 29 bar. Confirmed cut by setting down 5 Ton on cut." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.2 hours. Operational details: Staged up pumps in increments of 200 liter/min. Displaced well to 1,40 sg OBM with 1320 liter/min, 67 bar." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Filled triptank and performed flowcheck, well static." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Pumped 4 m3 - 1,70 sg slug." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 530m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: POOH with 13 3/8' casing cutting BHA on 5 1/2' DP from 1422 m to 530 m. Average tripping speed 1189 meter/hr." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 530m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Filled triptank with 1,40 sg OBM." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 26m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH with 13 3/8' casing cutting BHA on 5 1/2' DP from 530 m to 26 m. Average tripping speed 1008 meter/hr. Meanwhile performed pre-job meeting prior to changing handling equipment." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 26m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed master bushings." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Broke out and laid down 13 3/8' cutting assembly." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Picked up and RIH with wearbushing RT and jetsub assembly. Jet washed WH with 3000 liter/min, 53 bar. Engaged wearbushing and pulled free with 37 ton overpull. POOH with wearbushing and jetsub assembly, laid down same." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to retrieve seal assembly" "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.8 hours. Operational details: Picked up and RIH with seal assembly RT and jetsub assembly. Jet washed WH with 3000 liter/min, 54 bar. Installed DPSV in string. Ran in and engaged seal assembly. Lined up on choke and closed annular preventer. Pulled seal assembly free and oberved well on choke, no pressure observed. Opened well and performed flowcheck on triptank, well static. POOH with seal assembly and RT, broke out and laid down same to cantilever. Broke out DPSV from string." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: Picked up and made up 13 3/8' casing spear assembly. RIH with spear assembly to 131 meter. Recorded up / down weights 80 / 76 Ton. Connected TDS, ran down and engaged 13 3/8' casing. Pulled 13 3/8' casing free with 25 Ton overpull. Continued to pull OOH to 139 meter." "On 2013-11-06, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to circulation. Meanwhile observed well on triptank." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.5 hours. Operational details: Circulated 13 3/8' x 20' annulus to 1,40 sg OBM with 2020 liter/min, 26-28 bar." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Flow checked well, static." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Pumped 4 m3 - 1,70 sg slug." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1284m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: POOH with 13 3/8' casing on 5 1/2' DP from 1422 m to 1284 m. Set hanger in slips. Picked up and released spear from hanger. Laid out spear assembly to cantilever." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1284m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.2 hours. Operational details: Rigged up 13 3/8' casing handling equipment." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1284m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crews." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1272m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: POOH 13 3/8' hanger, broke out and laid down same." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 823m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 5.2 hours. Operational details: POOH with 13 3/8' casing from 1272 m to 823 m. Average pulling speed 7,1 joints/hr." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 823m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Checked and serviced casing handling equipment." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 618m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: POOH with 13 3/8' casing from 823 m to 618 m. Average pulling speed 11,4 joints/hr." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 618m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Serviced and lubricated casing handling equipment." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 5.5 hours. Operational details: POOH with 13 3/8' casing from 618 m to surface. Average pulling speed 9,4 joints/hr." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: Rigged down casing handling equipment." "On 2013-11-07, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: Picked up seal assembly RT with 'used' seal assembly (White painted). RIH with seal assembly to below BOP. POOH with seal assembly and inspected same, no damage observed. RIH with seal assembly to 137 meter, hang up on shear seal, sat down 12 Ton." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: POOH with 'used' seal assembly and inspected same, no damage observed." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.8 hours. Operational details: Picked up new seal assembly and RIH from surface to 139,2 meter. POOH with seal assembly and inspected same, no damage observed." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: RIH with seal assembly from surface to 140,38 meter. POOH with seal assembly." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Inspected seal assembly, found vertical marks on the seal OD. Broke out and laid down seal assembly RT." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Picked up and made up wear bushing running tool and jet sub." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: RIH with wear bushing. Jet washed WH with 2900 liter/min, 57 bar. Installed wearbushing. POOH with wearbushing and jetsub assembly RT, laid down same." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: Picked up 13 3/8' casing cutter assembly from cantilever and broke off 5 1/2' HWDP single." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Held pre-job meeting prior to slip & cut drill line. Slipped and cut drill line. Cleaned and cleared rig floor." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 5m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Made up 5 meter 5' DP pup with centralizer to 5 1/2' DP stand. Installed PS-21 slips." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1340m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: RIH with 5 1/2' DP cement stinger from 5 m to 1340 m. Average tripping speed 890 meter/hr." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1418m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.8 hours. Operational details: Connected TDS and washed down from 1340 meter with 500 liter/min, 5 bar, 3-15 % gas. Started degassers. Observed obstruction at 1418 meter, not able to pass through. Increased pump rate in increments of 200 liter/min to 2000 liter/min, 15-31 bar, 6-12 % gas." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1418m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Attempted to work string past 1418 meter with 2000 liter/min, 31 bar, 1,7-8,0 % gas, 0-20 Ton. Observed pressure increase to max 50 bar." "On 2013-11-08, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1418m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.5 hours. Operational details: Continued to circulate to decrease gas level. Circulated with 2500 liter/min, 42-45 bar, 1,7-0,3 % gas." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1418m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Circulated with 2500 liter/min, 42-45 bar, 0,45-0,18 % gas. At 01:00 established rotation with 40 rpm, 2-4 kNm. Performed pre-job meeting prior to cement job." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1417m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Racked back stand and made up pump in sub with DPSV above and below. Meanwhile monitored well on triptank, well static." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1417m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Hooked up surface lines and pressure tested same to 200 bar for 10 minutes." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1417m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Pumped 26,9 m3 of 1,60 sg spacer at 2215 liter/min, 10-35 bar. Mixed and pumped 22,6 m3 of 2,0 sg cement slurry at 640 liter/min. Displaced cement to the rig floor with 890 liter drill water. Zeroed stroke counters. Pumped 1,9 m3 of 1,60 spacer. Displaced cement with 12,4 m3 OBM at 2200 liter/min, 5-10 bar, 50 rpm, 3-5 kNm." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1348m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.8 hours. Operational details: Broke out pump in sub with DPSV above and below. POOH to 1348 meter. Dropped two sponge balls. Circulated clean with 3330 liter/min, 61 bar, 50 rpm, 3-6 kNm. Dumped 63 m3 contaminated mud." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1348m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Flow checked well, ok." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1295m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH wet with 5 1/2' DP stinger from 1348 m to 1295 m." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1295m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 4 m3 - 1,70 sg slug." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: POOH with 5 1/2' DP stinger from 1295 m to surface. Average tripping speed 863 meter/hour. Filled trip tank from 08:05 to 08:10 hrs." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed PS-21 slips and installed master bushings." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Broke out and laid down cement assembly with pump in sub and DPSV's." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Picked up and RIH with wearbushing RT and jetsub assembly. Jet washed WH with 3050 liter/min, 55 bar. Engaged wearbushing and pulled free with 20 ton overpull. Confirmed measurement to WH. POOH with wearbushing and jetsub assembly, laid down same." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to mill run." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Picked up and made up mill assembly. RIH with mill assembly on 5 1/2' HWDP from surface to 139 meter. Made up TDS and established circulation at 1000 liter/min, 7 bar." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Polished WH area from datum at 138,9 m to 139,3 m with 400 - 1000 liter/min, 6-9 bar, 30 rpm, 1-2 kNm." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: POOH with mill assembly on 5 1/2' HWDP from 139 m to surface and laid out same." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Picked up seal assembly and RIH from surface to 140,3 meter. POOH with seal assembly and inspected same, observed vertical marks on the seal OD." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: RIH with wear bushing. Jet washed WH with 2900 liter/min, 57 bar. Installed wearbushing. POOH with wearbushing and jetsub assembly RT, laid down same. Cleaned and cleared rigfloor." "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to making up BHA" "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Picked up and made up 17 1/2' drilling BHA and RIH from surface to 25m" "On 2013-11-09, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Plugged i and programmed MWD tool" "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 25m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Plugged in and programmed MWD tools." "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 112m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: Picked up DC`s, jar and accelerator. RIH with 17 1/2' BHA from 25m to 112m" "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 234m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' HWDP from 112m to 234m." "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 234m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushings and installed PS-21 slips." "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1271m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 234 to 1271m." "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1271m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Filled pipe" "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1271m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed choke drill" "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1351m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Washed down with 17 1/2' bha from 1271m to 1351m at 2500 liter/min, 105 bar. Tagged firmed cement at 1351 meter" "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1351m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed downlink with 3600 liter/min, 220 bar" "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1373m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Drilled cement from 1351m to 1373 m with 3000-3810 liter/min, 155-230 bar, 122 rpm, 11-17 kNm, ROP 12-14 m/hr, WOB 3-5 ton, ECD 1.437 sg, Max gas 0,02 %." "On 2013-11-10, at Well NO 15/9-F-15 C, a drilling event occurred at a depth of 1380m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: Continued to K/O from F-15 C to F-15 D. Drilled with reduced rate from 1373m with 3000-4010 litre/min, 155-237 bar, 122 rpm, 6-12 kNm, ROP 2-5 m/hr, WOB 3-5 ton, ECD 1,438 sg, Max gas 0,04% At 14:00 hrs, 1380m MD, 50% cuttings was observed *****Reporting continued on F-15 D******" "On 2007-09-14, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: WOW to skid rig to F-7. Wind 41-53 kt." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: WOW to skid rig to F-7. Wind 41-53 kt." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 2.5 hours. Operational details: Held tool box meeting prior to skidding. Removed main staircase and baskets to be able to skid. Skidded rig to F-7. Had decreasing trend on weather (wind 25-38 kt, morning forcast 17-22 kt) and decided to to skid all the way out to remove riser tie-in winch." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Starboard aft skidding cylinder failed and thus stopped skidding operation. Decided to cancel skidding operation to remove riser tie-in winch and to stay on location (F-7) and start drilling." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.2 hours. Operational details: Installed stairways to cantilever. Removed diverter and riser equipment from drill floor." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Held tool box meeting before pipe handling. LO 12 singles of 5 1/2' HWDP. LO 3 singles of 8 1/4' DC." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Changed dies on aft PRS." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.2 hours. Operational details: Continued to LO 3 singles of 8 1/4' DC. PU and MU 3 stds of 5 1/2' HWDP and RB in derrick as dedicated landing string." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Serviced TDS and blocks." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 9m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: PU 36' HO assembly. Removed master bushing and outer ring. RIH with 36' HO assembly to 9 m and re-instated outer ring and bushing." "On 2007-09-15, at Well NO 15/9-F-7, a drilling event occurred at a depth of 17m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: MU 36' BHA from 9 m to 17 m." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: MU 36' BHA from 17 m to 26 m." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 26m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Skidded cantilever 11 cm forward to adjust rig floor on F-7." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: MU 36' BHA from 26 m to 122 m." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Performed derrick inspection prior to spudding the hole. Meanwhile ROV checked template and got in position for stab-in." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: MU 36' BHA from 122 m to 144 m. Observed fill below template. Continued RIH slowly without pumps and with no rotation until positive tag at 145.0 m." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Started pumping seawater at 1000 lpm and washed down with no rotation." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: No progress washing down at 1000 lpm with no rotation due to cement below template. Evalutated situation of having centralizer drill bushing at F-12 DCI level. Decided to change BHA to be able to drill out cement." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: POOH to change BHA." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: PU and MU 26' BHA" "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RIH with 26' BHA to 142 m. ROV assisted stabbing into template guide funnel. Washed down with seawater to 145 m with 550 lpm." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled cement with seawater at 550 lpm/4-5 bar, 5 rpm/1-2 kNm and 1 MT WOB to 149 m. 4 m drilled hole will allow centralizer drill bushing to land in template guide funnel when starrting to drill with 36' HO assembly." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH with 26' BHA from 149 m to surface." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: Performed software upgrade on VI-CIS. Meanwhile serviced PRS and rig floor equipment." "On 2007-09-16, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: PU 36' HO assembly." "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: Removed master bushing and outer ring. RIH with 36' HO assembly to 9 m and re-instated outer ring and bushing. MU 36' BHA from 9 m to 142 m. Stabbed into funnel on template guided by ROV and washed down 600 lpm/1 bar to 145 m." "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Attempted to enter 26' hole washing down 600 lpm/1 bar. Inspected string with ROV and found that 36' HO and centralizer bushing was clear of F-12 DCI. Applied 1-5 rpm and entered pre-drilled 26' hole. Washed down 1000 lpm/1 bar to 149 m. Observed with ROV that centralizer bushing had not landed out in funnel." "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Reamed 26' pre-drilled hole to be able to land out centralizer bushing in funnel, 1000-1500 lpm, 5-15 rpm." "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 187m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled 36' hole from 149 m to 187 m MD, 2000-4550 lpm, 15-83 bar, 50-80 rpm, 4-7 kNm, 1-2.5 MT WOB, ROP 5-9 m/hr. Pumped 20 m3 hi-vis pills as required. Down linked and performed survey at 168 m and 183 m. Up weight 102 MT / Down weight 97 MT. Survey at 155 m 0.93 inc at 171 m 0.49 inc. at 184 m 0.57 inc" "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 187m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired liner spray on mud pump #3." "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 209m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 36' hole from 187 m to 209 m MD, 4550 lpm, 83 bar, 80 rpm, 4 kNm, 1-2.5 MT WOB, ROP 5-9 m/hr. Pumped 20 m3 hi-vis pills as required. Down linked and performed survey at 197 m. Survey at 195.6 m 0.49 inc" "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 207m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated btms up with seawater and sweept with 25 m3 hi-vis pill. ROV confirmed TD by measuring paint mark 0.5 m below template funnel. Displaced hole to 1.40 sg bentonite mud at 4800 lpm and 106 bar." "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: POOH with 36' BHA from 206 m to 5 m below seabed. No drag observed. Topped up hole with 1.40 sg mud at 1770 lpm and 5 bar. POOH with 36' BHA and LO same." "On 2007-09-17, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared and tidied rig floor off excess equipment. Held tool box meeting prior to picking up CART assembly." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: PU CART assembly and RB in derrick. MU cmt assembly and LO same. Removed 5 1/2' elevators and bails. RU for running 30' conductor." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box meeting with all personnel involved prior to running conductors. PU 30' shoe joint and checked float for flow through by flushing with water." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: MU 30' conductor. Installed cement top-up system with cement oulet 25 m below mud line and burst disk assembly 15 m below mud line. Aligned UWG top-up system to avoid conflict with the 3 hydraulic rams in the template well slot." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Changed 5 1/2' DP elevator and bails. Re-installed link tilt system." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: MU conductor housing joint. Landed out on bushing in rotary. Disconnected and LD handling CART." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RU innerstring C-plate on top of 30' housing joint. MU up aluminium cement stinger (innerstring). PU CART and stabbed lower end into innerstring x-over. Removed C-plate. Locked CART to housing joint with 5 left-hand turns. Performed PU test. Installed 2' fill up valve and inclinometer on CART." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Ran conductor through rotary and installed master bushings. Installed cement top-up system as conductor was RIH." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed hose for UWG top-up system." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Filled conductor with SW and continued RIH with 30' conductor on 5 1/2' HWDP landing string to 118 m." "On 2007-09-18, at Well NO 15/9-F-7, a drilling event occurred at a depth of 118m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed dies on pipe handler." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 118m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed dies on pipe handler." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 30' conductor on 5 1/2' HWDP landing string from 118 m to 138 m." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Stopped RIH with 30' conductor at 138 m due to possible collision with F-12 DCI valve. Monitored and evalutated situation." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RU tugger from moonpool and installed wire sling on lower part of conductor with ROV to manipulate 30' conductor away from F-12. String weight 105 MT." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 30' conductor on 5 1/2' HWDP landing string past F-12 DCI valve and stabbed into template slot assisted by ROV." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 157m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 30' conductor on 5 1/2' HWDP landing string from 143 m to 157 m." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 30' conductor on 5 1/2' HWDP landing string from 157 m to 203 m." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Spaced out cement stand and ensured that 30' conductor housing was 112.88 m from machined ring on centralizer deck. ROV checked level using DigiQuartz. Found F-7 to be 27 cm to high. Adjusted string hight and checked level with DigiQuarz. Made two measurements and confirmed F-7 to be positioned 12,2 cm higher than F12, as per program." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Ran in with forward 6 MT tugger as guide from moonpool. ROV hooked it up to the template and attached shackle and rope to the hot stab. Launched the minireel hose from moonpool on the guide tugger. Hooked up ROV with hydraulic reservoir to hydraulic receptacle on template. Engaged centralization rams in template funnel. Pitch and roll readings : Before engaging rams ; roll 0.6 / pitch 0.2 After engaging rams ; roll 0.5 / pitch 0.2" "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated 30 m3 SW at 2500 lpm. Meanwhile held tool box talk prior to cement job." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Trouble shoot purge system prior to cement job." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Mixed and pumped 46.2 m3 1.52 sg Tuned Light XL cement slurry at 800 lpm. Displaced cement slurry with 6.0 m3 of SW at max rate using cement unit. Bleed off pressure and checked for back-flow. Removed cmt hose and flushed through manifolds and hoses." "On 2007-09-19, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 6.8 hours. Operational details: WOC while holding landing string in tension at correct depth. Meanwhile: -Flushed and cleaned cmt unit. -Inspected seabed for sement returns - inconclusive due to poor visability -Performed maintenance on aft PRS -Prepared for Top-up job" "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: WOC while holding landing string in tension at correct depth." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box meeting in cement control room prior to pumping down the top-up pipe. Lined up to to pump down top-up pipe. Tested line and manifold 100bar/5 min. Stepped up pressure pumping at 50 l/min. At 52 bar (770 psi) differential, pressure bled of rapidly indicating burst disk rupture. Indications are that it is the shallowmost disk that ruptured." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Performed circulation test at 500 lpm/32 bar with SW for 10 min. Prepared for remedial cement job. Pumped 6 m3 of 1,56 G-cement slurry at 500lpm/74 bar. Displaced cement down cement hose and top up pipe with 1,1 m3 SW." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Disconnected hose and dropped release ball. Let ball drop and sheard out release sub on UWG with 139 bar. Checked release by ROV." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Attempted to retrieve UWG top-up hose. Flushed hose with 5 m3 SW. Took weight with tugger, but were unable to pull the released hose out of the top-off system." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: Installed cutter on ROV. Cut UWG top-up hose and retrieved it to surface." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 31m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Slacked off to neutral weigt. Observed no movement on conductor. ROV confirmed inclinometer readings. Released CART by rotating 5 times to the right. Pulled CART above 30' housing. RB 1 std and dropped sponge ball and flushed DP with 2500 lpm for 5 min. POOH. Meanwhile attempted to retract centralization rams in template funnel. ROV did not manage to pull dummy hot-stab and broke handle on operation panel. Pitch and roll readings : After cement job; roll 0.43 / pitch 0.54" "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 31m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box meeting befor handling BHA. LO cement stinger and CART." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pulled vacuum hose for DCI through rotary for ROV to pick up." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: BO and LO cement stand. RD 6 MT tugger in moonpool. Cleaned and cleared rig floor." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Held tool box talk with all personnel involved. PU 17 1/2' bit and motor assy." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: BO pre-made bit and mudmotor assembly and adjusted bend to 1.22 deg. MU bit and motor assembly." "On 2007-09-20, at Well NO 15/9-F-7, a drilling event occurred at a depth of 9m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: MU and RIH with 17 1/2' BHA." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 144m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: MU and RIH with 17 1/2' BHA from 9 m to 129 m. Stabbed into 30' conductor housing at 139.7 m assisted by ROV. RIH with 17 1/2' BHA to 144 m." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 188m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: MU and RIH with 17 1/2' BHA from 144 m to 188 m. Started circulating and attempted to take survey without sucess." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 188m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: RB 1 std and topped up oil in TDS." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 188m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Attempted to re-take survey without sucess." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 210m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Washed down and tagged cmt at 196 m. Drilled out shoe from 196 m to 210 m; 3500 lpm, 93 bar, 60 rpm, 3 kNm, 2 MT WOB. Up weight 100 MT/down weight 97 MT. Pulled through shoe and observed no drag." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 215m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Attempted to re-take survey without sucess. Drilled 17 1/2' hole from 210 m to 215 m; 3000 lpm, 71 bar, 60 rpm, 1-6 kNm, 1 MT WOB. Attempted to re-take survey without sucess." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 215m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated while evaluating problem with survey. Spotted 10 m3 1.40 sg pill on bottom prior to POOH to change BHA." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: POOH from 215 m to 192 m. Inspected TDS for loose items. Continued POOH from 192 m to surface." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Changed 5 1/2' elevator due to missing pin." "On 2007-09-21, at Well NO 15/9-F-7, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: MU and RIH with new 17 1/2' BHA to 36 m." "On 2007-09-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: MU and RIH with new 17 1/2' BHA from 36 m to 129 m. Stabbed into 30' conductor housing at 139.7 m assisted by ROV. RIH with new 17 1/2' BHA from 140 m to 200 m. Weight under jar is 13 MT." "On 2007-09-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 200m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: RU gyro unit in V-door to be able to run single shot survey through DP." "On 2007-09-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 200m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: Changed electrical box in gyro unit." "On 2007-09-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 200m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Continued RU gyro unit in V-door to be able to run single shot survey through DP." "On 2007-09-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 215m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Washed down from 200 to 215 m. Pulled back through shoe to verify no obstruction." "On 2007-09-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 266m. The activity was categorized as 'drilling -- drill' and lasted for 14.2 hours. Operational details: Drilled 17 1/2' hole from 215 m to 266 m using 5 1/2' HWDP as drilling stand; 3100-3400 lpm, 75-87 bar, 60 rpm, 1-6 kNm, 1 MT WOB. Up weight 97 MT/down weight 93 MT. Pumped 10 m3 hi-vis sweep and spotted 10m3 hi-vis on bottom prior to each gyro run. Performed gyro survey every single drilled. Strapped pipe to one side at centralizer deck using 6 MT moonpool tugger to enhance quality on survey. Gyro kept hanging up while RIH at 110 m from bit (inside 5 1/2' HWDP) and needed several attempts to be able to pass." "On 2007-09-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 276m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 17 1/2' hole from 266 m to 276 m; 3000-3500 lpm, 60-92 bar, 70 rpm, 2-5 kNm, 3-5 MT WOB. Pumped 10 m3 hi-vis sweep and spotted 10m3 hi-vis on bottom. Performed gyro survey at 262 m." "On 2007-09-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 276m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Dropped T-bar (2.5 cm x 2.5 cm extended screw) from gyro goose-neck. It was probably lost down hole (inside drill string). Evaluated situation and discussed further action with town, decided to continue drilling operation." "On 2007-09-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 280m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Performed gyro survey at 273.4 m. Drilled 17 1/2' hole from 276 m to 280 m; 3500 lpm, 98 bar, 70 rpm, 3-4 kNm, 3-4 MT WOB." "On 2007-09-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 307m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled 17 1/2' hole from 280 m to 307 m using 5 1/2' HWDP as drilling stand; 3000-4000 lpm, 76-126 bar, 70 rpm, 1-6 kNm, 2-4 MT WOB. Up weight 100 MT/down weight 97 MT. Pumped 10 m3 hi-vis sweep and spotted 10m3 hi-vis on bottom prior to each gyro run. Performed gyro survey every single drilled." "On 2007-09-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 307m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 10 m3 hi-vis pill and swept out of hole. Spotted 12 m3 1.40 sg mud at 3100 lpm/72 bar." "On 2007-09-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: POOH from 307 m to 122 m. No drag observed. Inspected TDS for loose items. Continued POOH from 122 m to surface. Found T-bar, that was lost yesterday from gyro goose-neck, in bit." "On 2007-09-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 83m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: MU and RIH with new 17 1/2' BHA from surface to 83 m." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with new 17 1/2' BHA from 83 to 122 m." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 122m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Surfaced ROV to repair hydraulic leak." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 227m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH with new 17 1/2' BHA from 122 to 129 m. Stabbed into 30' conductor housing at 139.7 m assisted by ROV. RIH with new 17 1/2' BHA from 140 m to 227 m." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 195m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Surfaced ROV to repair hydraulic leak in operation-arm. Meanwhile pulled 171/2' BHA into shoe at 195 m. Dived ROV and re-connected on to DCI hose." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 305m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH with new 17 1/2' BHA from 195 to 305 m. Attempted to take survey at 305 m with gMWD before drilling ahead." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 308m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Continued attempting to take survey with gMWD at 307 m without sucess. Drilled 1 m to 308 and made several attempts to take survey. No sucess. MWD transmission is working fine, but gMWD signals are corrupt." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 308m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Continued attempting to take survey with gMWD at 308 m without sucess. MWD transmission is working fine, but gMWD signals are 'froozen' (will not create new signals)." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 308m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 10 m3 hi-vis pill and swept out of hole. Spotted 12 m3 1.40 sg mud prior to POOH." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: POOH from 308 m to surface. No drag observed." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: Changed out gMWD tool." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 261m. The activity was categorized as 'drilling -- trip' and lasted for 5.8 hours. Operational details: MU and RIH with new 17 1/2' BHA from surface to 136 m. Stabbed into 30' conductor housing at 139.7 m assisted by ROV. RIH with new 17 1/2' BHA from 140 m to 261 m. Sat scribe-line and aligned UHBO. Surface tested gMWD at 49 m, 3100 lpm/65 bar." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 308m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Washed down with new 17 1/2' BHA from 261 to 308 m, 3100 lpm, 80 bar, 60 rpm, 1-5 kNm. Attempted to take survey at 298 m and at 308 m with gMWD before drilling ahead." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 328m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Drilled 17 1/2' hole from 308 m to 318 m; 4000 lpm, 131 bar, 70 rpm, 1-5 kNm, 0-1 MT WOB. Attempted to take survey with gMWD without sucess. Drilled 17 1/2' hole from 318 m to 328 m and attempted to take survey with gMWD without sucess." "On 2007-09-24, at Well NO 15/9-F-7, a drilling event occurred at a depth of 328m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RB 1std. Picked up 1 std of 5 1/2' HWDP to use as drilling stand." "On 2007-09-25, at Well NO 15/9-F-7, a drilling event occurred at a depth of 353m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' hole from 328 m to 353 m using 5 1/2' HWDP as drilling stand; 4000 lpm, 139 bar, 70 rpm, 2-5 kNm, 1-2 MT WOB. Up weight 102 MT/down weight 100 MT. Pumped 10 m3 hi-vis sweep and spotted 10m3 hi-vis on bottom prior to each WL gyro run. Performed WL gyro surveys at 331m, 339m, and 353 m. Each run taking approx. 1 hr incl. RU and RD." "On 2007-09-25, at Well NO 15/9-F-7, a drilling event occurred at a depth of 458m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 17 1/2' hole from 353 m to 650 m; 4000-4500 lpm, 141-177 bar, 80 rpm, 4-8 kNm, 4-6 MT WOB, ROP 35-70 m/hr. Pumped 3 x 10 m3 hi-vis sweeps and reamed one single pr std. Performed gyro survey every 30 m until more than 15 m away from F-12. Performed gyroMWD survey every std (approx every 40 m) from there on. Slided in following intervals: 480-495m, 530-538m, 560-570m, 595-610m, 632-650m. Meanwhile inspected TDS and derrick for loose items. Checked die-carriers. Carried out repairs on forward PRS. Pressure tested BOP (6 months tests)." "On 2007-09-26, at Well NO 15/9-F-7, a drilling event occurred at a depth of 759m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled 17 1/2' hole from 650 m to 759 m; 4000-4500 lpm, 130-160 bar, 80 rpm, 1-3 kNm, 3-4 MT WOB, ROP 33-55 m/hr. Pumped 3 x 10 m3 hi-vis sweeps and reamed one single pr std. Performed gyroMWD survey every std. Slided in following intervals: 675-690m, 745-760m. Up weight 114 MT/down weight 109 MT. Continued repairs on forward PRS and pressure tested BOP (6 months tests)." "On 2007-09-26, at Well NO 15/9-F-7, a drilling event occurred at a depth of 759m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Rotated and reciprocated pipe while repairs are carried out to MP1 and MP3." "On 2007-09-26, at Well NO 15/9-F-7, a drilling event occurred at a depth of 759m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Rotated and reciprocated pipe while repairs was carried out to MP2 and MP3." "On 2007-09-26, at Well NO 15/9-F-7, a drilling event occurred at a depth of 915m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: Drilled 17 1/2' hole from 759 m to 915 m; 4440-4515 lpm, 168-173 bar, 80 rpm, 3-8 kNm, 1-7 MT WOB, ROP 45-90 m/hr. Pumped 3 x 10 m3 hi-vis sweeps and reamed one single pr std. Performed MWD cluster at 800 m and gyroMWD survey every std. Slided in following interval: 907-915m. Up weight 122 MT/down weight 115 MT." "On 2007-09-26, at Well NO 15/9-F-7, a drilling event occurred at a depth of 915m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Pumped 30 m3 hi-vis followed by 30 m3 SW and then 30 m3 hi-vis to circulate hole clean, 3500 lpm, 107 bar, 30 rpm. Pulled 1 std and pumped 3 x btms up with SW, 4450 lpm, 159 bar, 80 rpm." "On 2007-09-26, at Well NO 15/9-F-7, a drilling event occurred at a depth of 906m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Displaced open hole (170 m3) to 1.40 sg mud, 4450-2970 lpm, max 103 bar, 20 rpm." "On 2007-09-26, at Well NO 15/9-F-7, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: POOH with 17 1/2' BHA. Took 29 MT overpull at 315 m. Worked the pipe up/down with 1.40 sg mud at 450 lpm and 30 rpm on the string. No drag observed when POOH trough tight spot the second time. Continued POOH to 30' conductor shoe at 202 m and topped up conductor with 22 m3 1.40 sg mud. Continued POOH and started laying out 17 1/2' BHA." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued laying out 17 1/2' BHA. Cleaned and cleared drill floor. Meanwhile prepared tugger for removing funnel." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RU for running 20 x 13 3/8' casing. Changed elevators and bails. Installed x-overs to Peak circ tool and installed flex hose." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Continued rigging up surface equipment prior to run 13 3/8' casing. Cleared and cleaned rig floor for casing running. Odfjell rigged up casing tong." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to running 13 3/8' casing" "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up and made up shoe joint, intermediate and landing collar joint and Baker locked same." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Put on guide line on casing shoe, to assist the ROV for guiding the 13 3/8' casing into the 30' conductor." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: RIH with 13 3/8' casing from 37 m to 137 m, filling the pipe every 5th joint. Laid out 2 joints of pipe." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: High pressure hose to port side pump of the ROV busted. ROV came out of the water, fixed busted hose and dived again." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Had several attempts to enter the 30' conductor with the 13 3/8' casing shoe before entering. Tuggers on centralizer deck and the ROV were used for guiding the 13 3/8' casing into the 30' conductor." "On 2007-09-27, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Continued RIH with 13 3/8' casing from 140 m to 536 m, filling the pipe every 5th joint." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 582m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Continued RIH with 13 3/8' casing from 536 m to 582 m. Laid out 3 joints of pipe." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 582m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: The casing tong were unable to make up high torque. Trouble shooted the casing tong, the tong were repaired and operation was resumed." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 773m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued RIH, with 13 3/8' casing from 582 m to 773 m, filling the pipe every 5th joint" "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 773m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to changing out surface handling equipment and picking up 18 3/4' well head." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 773m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Started rigging down the casing handling equipment." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 773m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued rigging down Odfjell surface equipment, elevator and bails. Rigged up bails and 5½' elevator." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 773m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk prior to picking up the 18 3/4' Well Head housing and CART assembly, and made up same." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 773m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged down the casing tong and the automatic slips and installed 5½' slips." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 908m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Ran in with 18 3/4' Well Head housing and landed same, took 25 MT over pull." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 908m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Circulation was established with sea water at 2300 lpm, prior to performing the cement job. Simultaneously tool box talk was held, and cement line tested to 200 bars 10 min." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 908m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: 20 bars were applied to the IBOP before commencing the cement job." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 908m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Mixed and performed cmt job. Pumped : 74,5 m³ 1.56 SG lead slurry at 900 - 1100 lpm, 14 - 18 bars pump pressure. 20 m³ 1.92 SG tail slurry at 800 - 1000 lpm, 13 - 18 bars pump pressure." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 908m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released dart, chased dart with 3000 ltr SW with cement unit. Top plug shear pressure/volume: 58 bars/1127 ltr. Continued displacing with rig pumps at 3000 lpm, slowed down to 1400 lpm after 52 m3 pumped. FCP 44 bars. At 2469 stks bumped plug, 97.7 % pump efficiency. Increased pressure to 114 bars and held for 10 min to pressure test casing.. Bled off pressure and checked for backflow to Halliburton cement unit, 640 l bled back." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 908m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Released CART assembly, pulled up 1 single and laid out cement head." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Dropped the two Halliburton sponge balls and flushed string using sea water at max rate. POOH. Pup joint and HWDP single were laid out, racked back remaining of the landing string in derrick. CART running tool was laid out." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Master bushing and adapter ring were removed. Installed rotary table frame barrier and lowered Tension ring assembly to Tension deck. Meanwhile flushed cement manifold lines. Installed master bushing and removed rotary table framed barrier." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up Cement head and broke of HWDP single and laid out same. Cleared and cleaned rig floor prior for next operation." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed riser saddle to HTS, rigged up for installing the rider spider." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk prior to run production riser." "On 2007-09-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up and made up handling sub for Tension joint and laid out same on cantilever." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: The riser spider were brought in to the rig floor." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Transported the riser spider to near the rotary, removed the master bushing and adapter ring. Installed the spider and hooked up hydraulic hoses and function tested same." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up TBC and stress joint and landed of in the spider." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up double riser number 1 and made up same. Riser was ran to a convenient height, for function testing of TBC in Moonpool area." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Vetco performed function test of the TBC according to the program." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Functioning test were continued of the TBC according to the program." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Continued too make up and ran in with production risers to 26.5m" "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk with day shift prior making up and running production riser." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 54m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Continued too make up and ran in with production risers to 54.5 m" "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 54m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Tension/guide wires were hooked up on the template using the ROV." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.8 hours. Operational details: Continued to make up and ran in with production risers to 103 m." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Flanges bolt on tension joint had to be cut from 415mm to 365mm." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Continued to make up the tension joint. Removed the riser spider and installed the master bushing. Started to run in with tension joint." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 120m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Tension joint got stuck in master bushing, 20 MT down weight. Picked up riser with master bushing attached to tension joint 10cm and were able to free bushing by hammering down the master bushing. No damage to the tension joint." "On 2007-09-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Tool box talk was held prior to stabbing/landing the TBC. Ran tension joint below rotary table and installed master bushing. Made up landing string to TDS. ROV removed the dust cover." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Aligned the TBC over the Well Head and ran down with the TBC over the Well Head." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Landed and connected the TBC as per Vetco procedure. Weight prior to landing 100 MT. Installed hot stab for locking the TBC set down 15MT. As moving the hot stab the umbilical came off the shackle attached to the guide line and the ROV lost the hot stab. The umbilical were pulled to surface and re-attached to the guide line and ran back in and connected up. Locked TBC as Vetco procedure." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Over pull 20 MT was held for 3 mins, adjusted tension to 10 MT as per Vetco procedure. Lined up to cement unit for pressure testing of the production riser found blockage in cement line." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: Investigated problem with cement/kill manifold lined up an alternative route." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Started to filling the riser prior to pressure testing of same." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Continued filling the riser prior to pressure testing of same. Pressure tested production riser 10/70 bars 5/10 mins. Volume pumped 560 litres had returns of 555 litres." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Vetco flushed TBC, installed dummy stab." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to installation of centralizers, tension ring assembly and tension cylinders." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Installed centralizers." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: Installed tension ring assembly and tension cylinders." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk with night shift prior to continue rigging the tension ring assembly and tension cylinders." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Continued rigging the tension ring assembly and tension cylinders. Adjusted tension cylinders to 150 MT." "On 2007-09-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box talk prior to rigging up the cutting device for cutting the production riser.Commenced rigging up the cutting device. Simultaneously removed and installed new drill line spool." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Continued rigging up cutting device for cutting the production riser. Simultaneously had the top drive serviced." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Cut the production riser 1360 mm above machined ring on Tension deck. Simultaneously serviced PRS." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled out landing string and broke out pup joints and landing sub." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Started bevelling of the production riser top. Rigged up slings for surface riser." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Bevelled the production riser top." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk prior to lowering down the surface riser and well head." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ran in with surface riser and well head according to Vetco procedure." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Measured new space out for correction of length for the surface riser." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pulling out with the surface riser." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled out with the surface riser and laid out same on cantilever." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Cut off 25 cm of the surface riser." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up surface riser and ran in with same, landed in well head. Pressure tested BT seal on the surface well head to 70 bars for 10 mins, took over pull of 2.5 MT." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Picked up and installed diverter, outer ring and master bushing." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up 12 ¼' drilling BHA." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Picked up 12 ¼' drilling BHA, ran in from surface to 37 m." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Problems with PRS trouble shooted, found soft ware problem, Eletronic Technician corrected error." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 175m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued RIH with 12 ¼' drilling BHA from 37 m to 175 m." "On 2007-10-01, at Well NO 15/9-F-7, a drilling event occurred at a depth of 175m. The activity was categorized as 'interruption -- maintain' and lasted for 1.8 hours. Operational details: Held tool box talk prior to changing out wash pipe, started to change out wash pipe." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 175m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Continued changing out the wash pipe, pressure tested same to 207 bars" "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Attempted to install 10' diverter elements, not possible due to damaged elements. Changed master bushing for PS 21 slips." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 880m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued RIH with 12 ¼' drilling BHA on 5½' DP to 859 m, made up to TDS, established circulation, washed down from 859 m with 1180 lpm 30 rpm. Tagged TOC at 880 m." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 881m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled cement/float from 880 m to 881 m with sea water 3060 lpm, 70 rpm and 84 bars." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 898m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Continued drill out shoe track from 881 m to 898 m, 3200 lpm, 99 bars, 70 rpm, 3-6 kNm, 2-3 MT WOB, pumped 20 m³ Hi-vis at 898 m." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 898m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Took out the PS-21 slips and installed the 10' diverter inserts, re-installed the PS-21 slips." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 916m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drill out shoe track from 898 m to 908 m 13 3/8' shoe. Drilled out rat hole from 908.m to 916.5 m, 3200.lpm, 100 bars, 70 rpm, 4 kNm, 1 MT WOB." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 916m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Cleaned rat hole. Held tool box talk prior to displace hole to WBM." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 916m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Displaced well to 1.28 SG Soludril-N WBM, 3200 lpm, 90 - 120 bars SSP. Density of mud in returns: 1,26 SG." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 959m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued to drill ahead from 916.5 to 959 m. 3200 lpm, 90 - 120 bars, WOB 1-10 MT, 70-180 rpm, torque 3-20 kNm. ECD 1.29 sg EMW. MP-1 shut down." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 959m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pulled off bottom circulating with MP-2, 1700 lpm, 42 bars SSP. MP-1 was re-started, the shut down caused by electrical error." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 970m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Continued to drill ahead to 970 m, stand pipe pressure dropped 40 bars." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 970m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Trouble shooted stand pipe pressure drop, tested/ checked MP-1 and MP-2, found no indication of surface error. Stand pipe pressure back to normal." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 978m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued to drill ahead to 978 m. Mud pumps shut down." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 978m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Circulated and reciprocated pipe, investigated MP-1 and attempted to repair same." "On 2007-10-02, at Well NO 15/9-F-7, a drilling event occurred at a depth of 978m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Attempted to establish drilling parameters. Mud pumps kept falling out." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 978m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued working on mud pumps." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 897m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pulled out and into the shoe, monitored well over the trip tank. Meanwhile continued working on mud pumps." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 897m. The activity was categorized as 'interruption -- repair' and lasted for 4.2 hours. Operational details: Investigated failures on mud pumps and carried out repairs. Failures located: MP-1: Swab in line, MP-2: Fluid end problems, MP-3: Liner problem, software problem, insufficient fluid supply." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 897m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Pepaired the mud pumps." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 978m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: circulated at 897 m to test pumps, Ran back in to 978 m." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1018m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled ahead from 978 m to 1018 m, 3300 lpm, 139 bars, 150 rpm, 10-12 kNm, WOB 9 MT, ECD 1.3 SG." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1018m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Took survey." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled ahead from 1018 m to 1083 m, 2880 lpm, 115 bars, 131 rpm, 12-18 kNm, WOB 6 MT, ECD 1.3 SG." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated bottoms up 3 times, reciprocating the pipe inside the shale, 3300 lpm 120 rpm. Flow checked well, well static." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 900m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Pulled up to inside the shoe at 900 m." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 900m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Flow checked well. Meanwhile held tool box talk prior to remove 10' diverter insert and removed same. Well static." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH from shoe and tagged TD at 1083 m, no tight spots." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated until well were clean, reciprocating the pipe inside the shale, 2700 lpm 96 bars." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flow checked well, well static." "On 2007-10-03, at Well NO 15/9-F-7, a drilling event occurred at a depth of 275m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: POOH with 5½' DP and 12 ¼' drilling BHA from 1083 m to 275 m, pulled out wet." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: Continued POOH with 5½' DP and 12 ¼' drilling BHA from 275 m to surface, pulled out wet and laid out 12 ¼' drilling BHA." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor prior to picking up clean out BHA." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Started to make up cleanout BHA." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 210m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Continued making up scraper BHA." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Held tool box talk with day shift. Ran scraper slowly through riser. Hung up at 87m. Picked up rotated string twice 90 deg. Attempted to pass obstruction. Discussed the situation with town. Meanwhile prepared for removal of the scaffolding in the derrick." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 210m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: POOH with 13 3/8' scraper. Removed PS-21 slips and installed master bushing. Inspected scraper." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 210m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held tool box talk prior to break/lay out scraper. Broke/laid out same. Removed master bushing and installed PS-21 slips." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1077m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Continued RIH with clean up BHA from 218 m to 1077 m, Took up/down weight at 1057 m 105/95 MT." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked up and made up Kelly cock and ball release sub. RIH to 1080 m." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated and increased pump rate in steps to 3000 LPM. String rotaion 40 RPM. Reciprocated the string while circulating." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Displaced 1,28 SG Soludril-N mud from open hole and +/-150 m into 13 3/8' casing. Pumped 43 m3 of 1.20 SG saturated NaCl brine at 3000 lpm/137 bar. Reciprocated the string while circulating." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Attached air control hose to the release ball sub and released 2 1/8' ball. Continued with displacement program, 400 lpm, 9 bar prior to shear the SABS sub. SABS sheared at 63 bar. 400 lpm/7 bar after." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Continued pumping to displace the 13-3/8' casing to 1.20 SG NaCl brine while rotating and reciprocation the string. Increased pump rate to 3000 lpm/34 bar after opening SABS. Pumped the High-vis soap train according to Halliburton procedure while reciprocating and rotating the string. Continued displacing the soap train with 1.20 SG NaCl brine until the well was clean." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Observed well for 30 mins, well static." "On 2007-10-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 130m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.2 hours. Operational details: Pumped 10 m³ 1.44 SG slug prior to POOH with clean up BHA. POOH with clean up BHA from 1080 m to 130 m" "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued POOH with clean up from 130 m to surface. Laid out bull nose. Metal shavings recovered with magnet." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Held tool box talk prior to perform drift run with liner hanger to 145 m." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 145m. The activity was categorized as 'completion -- sand control' and lasted for 2.5 hours. Operational details: Performed drift run with liner hanger to 145 m. No obstruction observed." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: POOH with liner hanger from 145 m to surface and laid out same, No marks or damage to the liner hanger re-runable." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Held tool box talk prior to rig up surface handling equipment for running 9 5/8' screens and casing" "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 1.8 hours. Operational details: Started rigging up surface handling equipment for running 9 5/8' screens and casing. Changed elevator inserts to 9 5/8' casing. Rigged up casing tong" "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 2.5 hours. Operational details: Continued rigging up for RIH with 9 5/8' screen." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Held tool box talk prior to picking up 9 5/8' screens. Picked up first joint and installed centralizer. Problems with torque set point on casing tong." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Investigated problems with torque set point on casing tong." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- maintain' and lasted for 4.0 hours. Operational details: Changed out the casing tong to the back-up tong. Function tested and calibrated the tong." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 47m. The activity was categorized as 'completion -- sand control' and lasted for 0.8 hours. Operational details: Continued to RIH with 9 5/8' screens from 12 m to 47 m." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 47m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Stopped RIH due to helicopter. No crane operation permitted." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 143m. The activity was categorized as 'completion -- sand control' and lasted for 2.0 hours. Operational details: Continued to RIH with 9 5/8' screens from 47 m to 143 m. Software problem with casing tong." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 143m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Trouble shooted the casing tong. Tong came out of sequence, due to software problem, repaired same." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 203m. The activity was categorized as 'completion -- sand control' and lasted for 1.8 hours. Operational details: Continued to RIH with 9 5/8' screens from 143 m to 203 m." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 212m. The activity was categorized as 'completion -- sand control' and lasted for 1.5 hours. Operational details: Held tool box prior to change out 5½' elevator inserts and pick up the liner hanger. Picked up liner hanger and made up same." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 212m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: Held tool box talk prior to rigging down 9 5/8' casing handling equipment. Started to rigging down 9 5/8' casing handling equipment. Not able to operate PRS." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 212m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Not able to operate the PRS. Electrical technician investigated and resat software." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 212m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: Completed rigging down 9 5/8' casing handling equipment." "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 212m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH with screens on HWDP and DP" "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 336m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: RIH with 9 5/8' screens on 5½' HWDP from 212 m to 336 m" "On 2007-10-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 500m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: Continued to RIH with 9 5/8' screens on 5½' DP from 336 m to 500 m" "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 907m. The activity was categorized as 'completion -- sand control' and lasted for 2.5 hours. Operational details: Continued RIH with 9 5/8' screens from 500 m to 738 m. Took weight at 738 m sat down weight 9 MT and picked up free. Made up TDS. Broke circulation 500 lpm, 5 bars, RIH passed obstruction at 738m. Continued RIH with 9 5/8' screens from 738 m to 907 m (shoe)" "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1060m. The activity was categorized as 'completion -- sand control' and lasted for 0.8 hours. Operational details: Continued to RIH with 9 5/8' screens in open hole from 907 m to 1060 m. Took up/down weight 124/105 MT" "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1062m. The activity was categorized as 'completion -- sand control' and lasted for 0.8 hours. Operational details: Dropped 1 3/4' aluminium ball. Positioned string at setting depth 1062 m in up weight. Chased ball with 220 lpm. Applied 125 bars to string when ball seated. Held pressure for 2 mins. Sat down weight 20 MT on liner hanger. Increased the pressure to 185 bars, 2 mins to released the running tool. Increased the pressure to shear the ball seat. Ball seat sheared at 200 bars. Picked up to the free moving up weight to bring the Packer Actuator dogs above the PBR. Sat down 30 ton. Observed packer shearing. Top Liner hanger PBR at 850 m." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 825m. The activity was categorized as 'completion -- sand control' and lasted for 1.8 hours. Operational details: Pulled running tool out of PBR to 825 m. Displaced 13 3/8' casing to 1.03 SG NaCl brine with 3000 lpm 45 - 35 bars." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: POOH with liner hanger running tool from 825 m to 810 m" "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 3.5 hours. Operational details: Continued to POOH with 9 5/8' liner hanger BHA from 810 m to surface and laid out same." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held tool box talk prior to change over from PS-21 to master bushing. Cleared rig floor and changed out PS-21 slips to master bushing. During installation of the master bushing the PRS tagged the pipe finger system. Visual inspection was performed and no visual damaged observed. During PU of Swab assembly, the aft upper PRS support arm came off and dropped on to the rig floor." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 9.0 hours. Operational details: Work was terminated until safe operation could continue. Both support arms were modified by installing safety wires. Double barrier" "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Time out with night shift discussed the incident." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: The PRS was function tested and accepted for continued operation." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Held tool box talk prior to pick up Swab assembly. Picked up SWAB assembly and tested check valve." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 848m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Changed to PS-21 slips. RIH with Swab assembly on 5½' DP from surface to 848 m. No losses to formation." "On 2007-10-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 848m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Made up to TDS. Swabbed in the well twice using 3 strokes at the time with stroke length of 35 m. Swabbing speed 30 m/min. Losses 400 and 1000 lpm." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 888m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Continued swabbing the well 3 times using 3 strokes at the time with stroke length of 35 m. Swabbing speed 40 and 50 m/min. Losses 1200, 700 and 600 lpm. Filled up trip tank and observed final loss rate of 300 lpm." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 888m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pressured up the string and bursted the burst disk sub at 250 bars." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with Swab assembly from 888 m to 1050 m." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 918m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Connected up to TDS POOH pumping 1000 lpm, 10 m/min, 8 bars SSP, 1.03 SG NaCl." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 829m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled the swab assembly above the PBR. Established a loss rate of 150 lpm." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 888m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Prepared for POOH with the Swab assembly." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 835m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Started to POOH with the Swab assembly from 888 m to 835 m." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 835m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Stopped POOH with the Swab assembly. Evaluated situation." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 835m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Held tool box talk with day shift. evaluated situation. Meanwhile greased drilling equipment, installed TIW." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 835m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.8 hours. Operational details: Slip and cut drill line." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 835m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Calibrated TDS height for Geoservices." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 112m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Started to POOH with 5½' DP and Swab assembly from 835 m to 112 m." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 112m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Picked and made up second Swab assembly." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 849m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: RIH with Swab assemblie from 112 m to 849 m." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued to RIH with Swab assemblie at 2 min/std to 1050 m." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Pumped 14,5 m³ of Citric acid (1,06 SG) with 1500 lpm. Displaced Citric acid with 8,6 m³ 1.03 SG NaCl brine at 1500 lpm. Closed DP on stand pipe valve, locked in fluid in DP. Let Citric acid soak." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 2 times with 10 m strokes 30 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 2 times with 10 m strokes 30 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 2 times with 10 m strokes 30 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 2 times with 10 m strokes 30 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m3 down DP and displaced clean acid into well bore." "On 2007-10-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Lined up to trip tank and established loss rate, loss rate 450 lpm." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1026m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Pulled the string up to 1026 m, having the upper swab cup inside the 9 5/8' blank pipe. Opened stand pipe valve. Pumped 30 m³ 1.03 SG brine, to ensure that the remaining Citric acid was bull headed into the formation. Pumping rate 420 lpm 5 bars SPP." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 900m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Pulled the string to 900 m having the bottom swab cup inside the 9 5/8' blank pipe. Displaced the remaining citric acid into the formation by pumping 20 m³ 1.03 SG packer fluid." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 840m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pulled the string up to 840 m above the PBR. Lined up to trip tank and established loss rate, loss rate 400 lpm." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 731m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: POOH with the Swabbing assemblies from 840 m to 731 m. As POOH filled the well with 1.03 SG packer fluid." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 731m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Stand threads got caught in box, when picking up with PRS. Freed the stand from box. Inspected the dies and the rollers on PRS head." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 530m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued POOH with the Swabbing assemblies from 731 m to 530 m. As POOH filled the well with 1.03 SG packer fluid." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Continued POOH with the Swabbing assemblies from 530 m to surface. Laid out the two Swabbing assemblies." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk prior to retrieving the bowl protector. Removed master bushing and pulled 18' diverter inserts." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH and retrieved the bowl protector at 20.61 m. POOH and laid out same. Installed the master bushing." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Made up the jetting tool. Ran in and washed the surface well head area (1500 lpm/5 rpm) total pumped 8 m³ packer fluid. Pulled out and laid out jetting tool." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Held tool box talk prior to perform dummy run with the tubing hanger. Cleared rig floor and picked up and made up tubing hanger. Ran in and landed the tubing hanger, documented the orientation. Pulled out with tubing hanger and racked back in the derrick." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 6.2 hours. Operational details: Held tool box talk prior to rig up. Rigged up surface equipment for handling the ESP equipment, casing tong, goose neck and cable." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Held tool box talk prior to picking up the ESP motor. Picked up same." "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Serviced the motor and evacuated the air" "On 2007-10-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Installed protector joint, ESP pump, discharge pressure assembly and x-o 9 5/8' x 7 5/8'." "On 2007-10-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Installed hydraulic line to Phoenix Multisensor at motor and leak tested connection to 207 bars (3000 psi) 10 min." "On 2007-10-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 4.8 hours. Operational details: Connected up the electrical cable to the motor and tested out same." "On 2007-10-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Continued testing of the cabling to the ESP motor." "On 2007-10-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Made up ¼' hydraulic line from Multisensor gauge to discharge pressure assembly. Leak tested 207 bar (3000 psi) for 10 minutes." "On 2007-10-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 16m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Held tool box talk prior to run in hole with 7 5/8' tubing. Changed slips inserts to 7 5/8' inserts." "On 2007-10-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 16m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Picked up 7 5/8' casing and adjusted Odfjell casing tong." "On 2007-10-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 500m. The activity was categorized as 'completion -- completion string' and lasted for 14.8 hours. Operational details: RIH with ESP on 7 5/8' tubing from 16 m to 500 m. Installed cable clamps every joint. Laid out 4 joints. Checked the Phoenix connection every hours." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 760m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: Continued RIH with ESP on 7 5/8' tubing from 500 m to 760 m. Installed cable clamps every joint. Checked the Phoenix connection every hours." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Continued RIH with ESP on 7 5/8' tubing from 760 m to 800 m. Installed cable clamps every joint." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Changed to 5½' DP inserts. Picked up, made up tubing hanger and installed cable clamp." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Rigged down the casing handling equipment and the casing tong." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Broke the fast connection. Orientated the tubing hanger by rotating hanger. Made up the fast connection to 17.7 kNm." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed the PS-21 slips and installed master bushing." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lower the tubing hanger down to suitable working height. Installed the penetrator in tubing hanger. Leak tested the penetrator o-rings to 69 bars (1000 psi) for 10 minutes." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Spliced the cable to pigtail, as per Schlumberger splicing procedure." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Checked the electrical connection and rigged down the splicing equipment" "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Rigged up and leak tested the penetrator o-rings to 69 bars (1000 ps)i for 10 minutes." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed the master bushing and ran in with the tubing hanger." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 826m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Checked the electrical connection. Installed the master bushing continued running in with the tubing hanger. Landed the tubing hanger at the mark from the dummy run. 20.61 m." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 826m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Disconnected the tubing hanger running tool by rotating the landing string to the right 9 turns. Pulled out the tubing hanger running tool." "On 2007-10-10, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: N/D the diverter and the riser and laid out the riser." "On 2007-10-11, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Prepared the surface Well Head for installation of the Tubing Bonnet, spacer spool and ball valve assembly. Installed same." "On 2007-10-11, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Leak tested cable penetrator seals in tubing bonnet to 69 bar (1000 psi). Meanwhile changed out valve on TDS." "On 2007-10-11, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Leak tested the tubing bonnet cavity to 69 bar (1000 psi)." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Well F-7 handed over from Production to D&W. Performed TBT for skidding rig with personnel from drilling, marine and technical departments." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Skidded the cantilever from F-9 to F-7" "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 4.0 hours. Operational details: Unbolted weather deck hatches on F-7. Moved split hatches in moonpool. Meanwhile prepared for nippling down flowline on F-7. Removed nuts on ball valve and prepared for lifting ball valve, spacer spool and tubing bonnet." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded cantilever from F-7 to F-9." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.0 hours. Operational details: Unbolted F-9 drilling hatches. Moved F-7 hatch to F-9. Meanwhile nippled down flowline on F-7 and prepared for lifting ball valve, spacer spool and tubing bonnet." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded cantilever from F-9 to F-7." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Installed split hatches on F-7." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Performed pre-job meeting for securing F-7 flowline on XMT deck." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.2 hours. Operational details: Secured flowhose with S-piece attached on XMT deck. R/U to pull tubing bonnet, spacer spool and ball valve. Vetco installed bolts for releasing lockring on tubing bonnet. Held TBT for running surface riser. Meanwhile Production Dept shut down adjacent wells according to SimOps-procedure." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Attempted to disconnect and pull tubing bonnet. Not able to pull assembly free." "On 2015-02-04, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 6.5 hours. Operational details: Attempted to disconnect tubing bonnet. Adjusted lockring releasing bolts. Worked tension 0-4 ton. Not able to move bonnet. Pressured up tubing bonnet cavity to pump tubing bonnet from below. Continued adjusting releasing bolts and working tension up/down. Tubing bonnet moved up, but slightly skewed. 4-5 mm movement close to the penetrator, 5-7 mm 180 degrees off the penetrator. Continued attempting to release tubing bonnet. Attempted to wiggle assembly horizontally with chain hoists connected to spacer spool at XMT deck. Installed hydraulick jacks to prevent tubing bonnet from dropping back down." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.8 hours. Operational details: Continued working tension up/down to release tubing bonnet. Managed to level out the travel evenly around bonnet. Slacked off tension and lowered soft slings to XMT-deck to remove braided wire slings and connect soft slings directly to ball valve. Dropped 1ea 2m 2 1/2' braided wire sling into tubing while disassembling. Evaluated situation and covered tubing." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: Connected soft slings to pad eyes on ball valve. Continued attempting to release tubing bonnet, working tension up/down while hammering on bonnet. Slowly making progress." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Tubing bonnet came loose. Removed latch ring releasing bolts. Pulled tubing bonnet, spacer spool and ball valve to drill floor. Covered tubing hanger with bucket." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Cleaned wellhead for landing surface riser. Meanwhile prepared surface riser for lifting." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Performed TBT for installing riser. P/U surface riser and tailed same into well centre. Lowered surface riser through rotary and latched on to surface wellhead. Production Dept informed re-start production from adjacent wells according to SimOps-procedure." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Performed TBT for installing diverter. P/U and nippled up diverter." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed master bushings. Changed handling equipment to 5 1/2'." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for releasing tubing hanger." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: P/U TH RT and M/U DP landing stand to same." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 827m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Measured in to to latch point 20,7 m and engaged RT by 9,5 left hand turns." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 827m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: R/U Weatherford tong. Meanwhile performed TBT for L/D tubing hanger." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 799m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed master bushings. Pulled tubing hanger free with nop overpull. Pulled tubing hanger above rotary." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 799m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Cut and terminated ESP cable, tested same. Meanwhile R/U compact auto slips and B/O tubing hanger." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 799m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: L/D down tubing hanger and running tool, assisted by crane." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 763m. The activity was categorized as 'workover -- completion string' and lasted for 1.5 hours. Operational details: POOH with 7 5/8' tubing with ESP cable from 799 m to 763m. Observed approx 30 cm of damaged armor cable." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 763m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Inspected cable. Lowered banana sheave from derrick to rig floor to allow damaged piece to pass through. Recovered parts of armor on next clamp on tubing. Approx 15 cm armor missing, presumably left in well." "On 2015-02-05, at Well NO 15/9-F-7, a drilling event occurred at a depth of 141m. The activity was categorized as 'workover -- completion string' and lasted for 8.8 hours. Operational details: POOH with 7 5/8' tubing with ESP cable from 763 m to 141 m. Avg pulling speed 5,8 joints/hr" "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 1.2 hours. Operational details: Continued POOH with ESP assemblies on 7 5/8' tubing from 141 m to 21 m. Avg pulling speed 5 joints/hrs. Recovered total 67 tubing clamps, no clamps left in hole." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: Performed TBT for changing handling equipment. Removed compact auto slips. Installed master bushings. Set manual slips on pup joint above discharge head." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: Pulled out to L/D ESP assemblies. Removed Protectorlisers down to Pothead. Cut ESP power cable. Attached ESP cable to rope with chinese finger and duct tape. Spooled back same over banana sheave up in derrick. With chinese finger in sheave, ESP cable came loose and dropped to rig floor." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Secured area. Evaluated situation. Performed TOFS." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT prior to continue operation." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 1.8 hours. Operational details: Pulled up to discharge head. Cut control line. Installed lifting clamp and landed on stovepipe. Removed bolt on head. Recovered dropped wire sling from top of discharge head. Continued B/O and L/D Discharge assy, Pump, Protector, Motor and Multisensor. Recovered total 4 ea Protectorlisers and 1 ea special XO clamp, no clamps left in hole." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor. Held TBT for R/U WL." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: R/U wireline equipment." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: P/U and M/U WL toolstring for multicaliper." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held TBT for running wireline operation. Tested toolstring." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 870m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: RIH with multifinger caliper toolstring to 870 m." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 15m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Opened caliper and started logging up from 870 m to surface." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Evaluated logging results. Meanwhile performed Time Out For Safety with all personnel involved in operation. Focused on use of established planning routines/TBTs, clear communication and the importance of stopping the operation if something is unclear, unsafe, or if there has been a change in conditions. Emphasised the general risk related to cold rig and campaign crew consisting of personnel gathered from various rigs." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Performed TBT for L/D WL toolstring. L/D same. Changed out cable head." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Prepared ME plug and setting tool. Meanwhile changed collar on Bolt on Head ESP-assembly." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for M/U ME-plug toolstring." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: M/U ME-plug toolstring. Charged up nitrigen chamber on setting tool." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT with night crew" "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Continued M/U ME-plug toolstring." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed operational checks and tested tools" "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 860m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: RIH with ME-plug on WL. Correlated depth in 9 5/8' screen hanger." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1048m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: RIH with ME-plug on WL. Lost weight at 1048 m. Pulled up and attempted to RIH at higher speed to pass obstruction. No go." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1046m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: P/U until tension in string. Activated setting tool and set plug according to Interwell procedure. Observed tension drop from 2230 lbs to 1520 lbs. RIH and tagged plug. Top plug at 1043 m. Mid element at 1044,2 m." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 1030m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed Time Out For Safety with all personnel involved in operation. Focused on use of established planning routines/TBTs, clear communication and the importance of stopping the operation if something is unclear, unsafe, or if there has been a change in conditions. Emphasised the general risk related to cold rig and campaign crew consisting of personnel gathered from various rigs." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: POOH with plug RT on WL to 50 m." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/D WL toolstring and R/D WL equipment." "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: L/D ME-plug RT" "On 2015-02-06, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: R/D wireline equipment. Cleaned and cleared rig floor." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Installed rotator arm on elevator. Installed #2 bowls." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed TBT for changing RT on primary TH assy." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Changed BX inserts to 9 5/8'." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: P/U primary TH/RT assy and landed same in rotary. Released running tool and L/D same. Attempted to P/U back-up TH/RT assy to land same in rathole. Malfunction on forward PRS" "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot foreward PRS." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: P/U back-up TH/RT and landed same in rathole. Released RT and installed same on primary TH in rotary. Meanwhile changed out ESP cable reel on catilever." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Performed TBT for L/D TH assemblies from rathole and rotary. L/D assemblies." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT for P/U and M/U ESP assemblies. Installed stovepipe above rotary." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: P/U ESP assembly 1 - Multisensor and motor. Landed lifting clamp on stovepipe in rotary. Serviced motor according to Schlumberger procedure." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 14m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: P/U and M/U ESP assembly 2 - Protector. Landed lifting clamp on stovepipe in rotary." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: P/U and M/U ESP assembly 3 - ESP pump. Landed lifting clamp on stovepipe in rotary." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Performed TBT with day crew." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: P/U and M/U ESP assembly 4 - Discharge pressure assembly. Landed lifting clamp on stovepipe in rotary." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Changed inserts in elevator to 7 5/8'." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: P/U and M/U assembly 5 - Bolt on discharge head." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Pulled back to multisensor and connected hydraulic line to same. Pressure tested hydraulic line to 3000 psi." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: RIH to top of motor. Tested motor and multisensor electrically. Megger tested cable" "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Mounted banana sheave for ESP power cable on PRS. Fed cable through same." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Spliced cable to connections on pump assembly." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Megger tested electrical cable to pump." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Serviced protector seal and filled with oil." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Installed protectorliser clamps on ESP assembly. Terminated hydraulic line. Landed and secured string with manual slips in rotary." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT for running 7 5/8' tubing with ESP power cable." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: P/U and M/U first 7 5/8' tubing joint. Fitted clamp on tubing collar. Installed compact auto slips." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 43m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: RIH with ESP assemblies on 7 5/8' tubing from 21 m to 43 m. M/U control line clamp on every connection." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 43m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with night crew for running 7 5/8' tubing with ESP cable." "On 2015-02-07, at Well NO 15/9-F-7, a drilling event occurred at a depth of 323m. The activity was categorized as 'completion -- completion string' and lasted for 4.8 hours. Operational details: RIH with ESP assemblies on 7 5/8' tubing from 43 m to 323 m. M/U control line clamp on every connection. Schlumberger megger tested power cable at 66 m and 173 m. Avg running speed 5,2 joints/hr." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 771m. The activity was categorized as 'completion -- completion string' and lasted for 5.8 hours. Operational details: RIH with ESP assemblies on 7 5/8' tubing from 323 m to 771 m. M/U control line clamp on every connection. Schlumberger megger tested power cable at 323 m, 455 m and 624 m. Avg running speed 6,9 joints/hr." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 771m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT for removing compact auto slips. Removed compact auto slips and installed master bushings. Meanwhile Schlumberger megger tested power cable." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 782m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: RIH with ESP assemblies on 7 5/8' tubing from 771 m to 782 m. Set manual slips. P/U and M/U 7 5/8' tubing pup joint." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 782m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for P/U tubing hanger. Changed elevator inserts to 5 1/2'." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 782m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: P/U TH/RT assembly from HTS." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 782m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT with day crew." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 792m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: B/O FAST connector. Oriented tubing hanger. M/U FAST connector." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 792m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH with tubing hanger to working height. Mounted penetrator in TH, measured cable cutting point. Disassembled penetrator and spaced out for cable splice. Performed final electrical checks on cable. Removed banana sheave from PRS." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 792m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: Cut cable and spooled back remaining cable to reel. Spliced cable to penetrator pigtails." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 795m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed penetrator in hanger, installed clamps on cable. Pressure tested penetrator seals, 69 bar / 10 min. Tested downhole system after splicing - ok." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 795m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed Vetco O-ring for tubing hanger. Removed master bushings." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 795m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: R/D Weatherford tong." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 819m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U DP landing stand, M/U same to TH RT. RIH and landed TH." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Disconnected RT. POOH with landing string." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Schlumberger tested ESP system through landing lead. Meanwhile performed TBT for nippling down diverter and surdface riser." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: L/D tubing hanger running tool." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed BX elevator. Installed chains and lifting bridle on TDS. Pulled master bushings." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled diverter, parked and secured same in set back. Verified adjacent wells shut-in according to SimOps-procedure." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Attached chains/slings to surface riser. Disconnected riser and pulled same to surface. L/D surface riser to HTS with crane assist." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Removed surface riser from HTS. Placed tubing bonnet/spacer spool/ball valve-assy on HTS. Meanwhile performed TBT for P/U and run assy." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: P/U, run and installed tubing bonnet/spacer spool/ ball valve-assy. Closed ball valve and disassembled pad eyes. Production Dept informed that heavy lift landed, according to SimOps-procedure." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Lifted flowhose with S-piece onto ball valve with tugger through rotary. Bolted flowline to ball valve. Bolts to be torqued-up at later stage by Production Dept. Simultaneously commenced pressure testing of penetrator seals in tubing bonnet, tubing bonnet cavity and annulus insert valve." "On 2015-02-08, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Installed hatch cover on F-7. Meanwhile continued pressure testing penetrator seals in tubing bonnet, tubing bonnet cavity and annulus insert valve." "On 2015-02-09, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.2 hours. Operational details: Continued pressure testing cable penetrator seals 69 bar / 10 min, tubing bonnet cavity 69 bar / 10 min and annulus insert valve 69 bar / 10 min. Meanwhile performed TBT and installed diverter and master bushings. Set TH RT with pup joint in foxhole, B/O and L/D same. Cleaned and cleared rig floor. --- END OF OPERATION @ 02:15 --- Commisioning to be performed offline" "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding to F-7" "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Finalized skidding checklists. Removed access stairs to cantilever." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded rig over well F-7." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Installed access stairs to cantilever." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling hatches on F-7." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Confirmed no pressure in well. Opened up bleed off valve and ball valve on well head." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled hatch." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Attached lifting arrangement for spool piece to TDS and tuggers using double securing. Adjusted lock ring on well head. Pulled spool piece to drill floor and L/O same." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed master bushing. Installed hatch cover in moonpool." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Cleaned and prepared seal area on well head. Meanwhile: Performed TBT P/U surface riser." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U surface riser from cantilever." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for running and landing surface riser on WH." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed master bushing and hatch cover in moonpool. RIH and landed surface riser on NT2 connector. Pulled 2 ton overpull, confirmed NT2 connector properly latched." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed lifting arrangement from TDS. Installed master bushing.. Meanwhile: Installed 'half moon' hatch around riser." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for diverter handling" "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U diverter from set-back. Observed chunks of cement in diverter overshot. Cleaned/washed same." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed diverter" "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed lifting arrangement from TDS bails. Installed 5 1/2' elevator." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for BHA handling" "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U Retrieval tool" "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 6m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ retrieval tool from surface to 6m." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 6m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew for continuing RIH with retrieval tool" "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ retrieving tool on 5 1/2' drill pipe to 20m. Enganged retrieving tool with 10 turns LH." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 6m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH w/ retrieving tool and completion string on 5 1/2' DP to 6 m and set slips on 5 1/2' pup. No overpull observed, up weight 97 ton." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 6m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for rigging up handling equipment and spooling unit for electrical cable to ESP." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 6m. The activity was categorized as 'plug abandon -- other' and lasted for 3.8 hours. Operational details: R/U casing handling equipment and spooling unit. Needed to move pipe from set-back to get enough space for spooling unit. Built shelter with scaffolding above spool operating panel." "On 2016-07-28, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with tubing hanger and installed FMS slips." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Continued rigging up FMS slips." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: B/O connection on tubing pup below TH and L/D TH and pup together." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 794m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/O tubing/completion." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 771m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH from 794 mMD to 771 mMD. Experienced issues with spooling unit rig-up. Alignment made it problematic to spool in at the same time as pulling out of hole." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 771m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: TOFS: Discussed rig up and red zone compliance. Decided to rig up cable sheave in PRS (2,5m above rotary) in order to minimize amount of work inside red zone." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 771m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Re-arranged rig up by including cable sheave. Installed sheave in PRS and rotated rotary 90 degrees to optimize alignment to spooler unit." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 579m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: POOH with tubing from 771 mMD to 579 mMD. Average pulling speed 5,7 jnt/hr." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 579m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew for L/O tubing" "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 528m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with tubing from 579 mMD to 528 mMD. Avg. pulling speed 6,6 jnt/hr." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 528m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for rigging down spooling unit and handling equipment." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 528m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: R/D handling equipment, scaffolding and spooing unit. Changed inserts in BX elevator, 5 1/2'." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 528m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U spear assy, inspected same and latched spear in tubing at surface." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 528m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Removed FMS slips and installed master bushing." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 864m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: RIH w/ tubing on spear and 5 1/2' DP from 528 m to 864 m . Avg. tripping speed 165 m/hr." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 864m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Sat down 20 ton and released spear." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH w/ spear on 5 1/2' DP from 325 m to surface . Avg. tripping speed 650 m/hr." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D spear assy" "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: P/U and M/U 13 3/8' EZSV plug BHA." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 286m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH w/ EZSV plug on 5 1/2' DP from surface to 286 mMD. Avg. tripping speed 286 m/hr." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 292m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Washed setting area with 600 lpm between 286 mMD to 292 mMD. Set EZSV plug at 289 mMD. Tagged plug with 10 ton." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 286m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Staged up pumps to 2900lpm. Pumped 18m3 SW. Disconnected TDS and pulled out 1 std." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 287m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: M/U pump-in sub. Spaced out with stinger at 287 mMD." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 287m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for placing balanced cement plug" "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 287m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed line test to 100 bar / 2 min. Bled back to 20 bar and confirmed line-up." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 287m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 2 m3 FW from cement unit. Mixed and pumped 7,8 m3 1,95sg cement slurry at 600lpm / 15 bar. Displaced cement with 2 m3 FW." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 287m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: L/D pump-in sub." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH with EZSV RT from 287 mMD to 170 mMD. M/U TDS, installed sponge ball and circulated above TOC. 2500 lpm /12 bar, 50 rpm / 5kNm." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 170 mMD to 3 mMD. Avg. tripping speed 640 m/hr." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: L/D EZSV RT." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Drained riser, bled off diverter system and prepared to pull diverter." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling diverter." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled diverter and R/B in set-back." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT rigging up to pull LP riser (surface riser)." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and attached lifting arrangement for LP riser." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for disconnecting LP riser." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Attempted to release connector on LP riser. Riser stuck, max overpull 8 ton." "On 2016-07-29, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Re-attempted to release connector." "On 2016-07-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Made several attempts to release LP riser connector. Re adjusted release bolts and attempted to move riser by extending/retracting TDS. Connector came loose after several attempts." "On 2016-07-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed hatch cover and liftet riser to drill floor and L/D same." "On 2016-07-30, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Rigged down lifting arrangement. Installed hatch plate on F-7. ************** End of report ***************" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Prepared for skidding. Completed pre-skid checklists." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding rig to F-7" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Skidded cantilever to well F-7." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Removed hatch in moonpool and built scaffolding in moonpool and WH decks. Meanwhile: Performed post-skid checks." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: PRS roller stuck on FWD PRS, troubleshot same." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with cutter BHA into wellhead. Issue with stuck roller on FWD PRS re-appeared. Decided to L/O Multibowl RT to free AFT PRS" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH with Multibowl RT. B/O and L/O 3 x pup 5 1/2' DP pups and singles (entire Multibowl RT BHA)." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U and M/U 2 std 5 1/2' DP and spear assy. RIH and M/U TDS. Engaged spear in riser. Pulled 20 ton overpull to confirm spear engaged." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Load shifted weight from tension system to TDS. R/D tension cylinders." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Installed diverter ('Stikhætta') on Multibowl. R/U hose for return flow. Removed boat collision stool." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled 30 ton over pull. Staged up flow rate to 2400 lpm / 95 bar. Cut riser at 134,5m." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Rigged down 'Stikhætta' and hose." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled riser and inner string to drill floor. R/U C-plate and landed off riser." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U false rotary and POOH with inner string, R/B same." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: P/U spear assy and engaged in riser. Changed out C-plate. Installed elevator and landed riser. Released spear and R/B. Removed BX-elevator and link tilt pins. POOH with riser (Lift #1), cleaned off marine growth on centralizer deck." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: R/U cutting machine. Cut riser. Significant wave height 1,4m R/D cutting machine." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: L/O tensioner joint and WH. Installed link tilt pins." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (Lift #2), cleaned off marine growth on centralizer deck." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 1,3m R/D cutting machine" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #2). Pulled riser (Lift #3), cleaned off marine growth at centralizer deck." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 1,6m R/D cutting machine" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O riser joint (Lift #3). Pulled riser (Lift #4), cleaned off marine growth at centralizer deck. Riser out of splash zone at 19:15" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. R/D cutting machine" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #4). Pulled riser (Lift #5), cleaned off marine growth at centralizer deck." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. R/D cutting machine" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #5). Pulled riser (Lift #6), cleaned off marine growth at centralizer deck." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. R/D cutting machine" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O riser joint (Lift #6). Pulled riser (Lift #7). L/O stress joint and lower pup joint." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for lifting tension cylinders from WH deck to drill floor." "On 2016-10-22, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lifted 8 ea tension cylinders from WH deck to drill floor." "On 2016-10-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued lifting remaining 8 ea cylinders from WH to drill floor. Removed scafflding in moonpool and WH decks." "On 2016-10-23, at Well NO 15/9-F-7, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed hatches in moonpool and WH decks **** END OF REPORT ****" "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Held tool box talk prior to skidding of the cantilever from F-14 to F-5" "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded the catilever from F-14 to F-5." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Started to re-establish rig condition for operation." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Installed handrails on weather deck and lower levels in well head modul." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Held tool box talk with day shift. Removed hatch cover from F-5 at well bay area. Failure on TDS." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Prepared and installed the rotating link adapter to TDS. Meanwhile removed hatch covers on F-14 prior to installing DCI stab for CRI hose." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed derrick inspection prior to start drilling 36' hole." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Held tool box talk. Picked up and made up the 36' BHA assembly. RIH with the 36' BHA. Meanwhile ROV prepared to install DCI stab for CRI hose." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Installed oil filter and solenoid valve to TDS. Function tested TDS, the rotating link adapter and torque wrench. Meanwhile prepared and connected DCI stab for CRI hose." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Serviced and inspected the TDS prior to start drilling the 36' hole. Prepared for moving drill cutting funnel from F-5." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Moved the drill cutting funnel from F-5. Using tugger and ROV." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 144m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: 36' BHA entered slot # 5 assisted by ROV." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Attempted to wash down 36' BHA through template. Drilled 36' hole from 144 m to 149 m MD. Drilling parameters : Flow 1000 lpm / SPP 4-5 bar / 18 RPM / Torque 3-12 kNm / WOB 1-10 MT. Drilling bushing landed out in template guide-funnel. Parked ROV in garage." "On 2007-11-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 155m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 36' hole from 149 m to 155 m MD. Drilling parameters : Flow 1000 lpm / SPP 2 bar / 20 RPM / Torque 2-4 kNm / WOB 1-2 MT / ROP 3,5 m/hr." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 164m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled 36' hole from 155 m to 164 m MD. Drilling parameters : Flow 1000-2200 lpm / SPP 2-15 bar / 20-70 RPM / Torque 2-9 kNm / WOB 2-3 MT / ROP 1-4.5 m/hr. Pumped 20m³ hi-vis pills prior to connection. Survey at 150.92 m 0.63 inc" "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 164m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Reamed hole from 164 m to 155 m Reaming parameters : Flow 3100 lpm / SPP 36 bar / 70-90 RPM / Torque 2-4 kNm 1. survey at 150.92 m 0.63 inc 2. survey at 150.92 m 0.57 inc" "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 36' hole from 164 m to 165 m MD. Drilling parameters : Flow 4000 lpm / SPP 66 bar / 90 RPM / Torque 2-6 kNm / WOB 0-1 MT / ROP 12 m/hr." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled 36' hole from 164m to 226m MD.(17½' bit depth) Drilling parameters: Flow 4000-4640 lpm / SPP 62-84 bar / 90 RPM / Torque 2-8 kNm / WOB 1-3 MT / ROP 6-18 m/hr. Pumped 20 m3 hi-vis pills prior to connection. Survey at 177 m 0.55 inc Survey at 187 m 0.47 inc Survey at 197 m 0.46 inc Survey at 207 m 0.27 inc Survey at 217 m 0.33 inc Survey at 225 m 0.26 inc" "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: TD with 17½' bit at 226m, TD 36' HO 222.8m. Circulated with sea water and pumped 25m³ hi-vis pills. Displaced well to 1.4 SG mud." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- ream' and lasted for 0.8 hours. Operational details: Held tool box talk prior to POOH. Started to POOH at 226m. Took 20MT overpull at 213m. Made up TDS and rotated pipe without pumping. Attempted to work through tight spot without rotation. Commenced to pump sea water at 1000 lpm and 30 rpm. Worked string reaming through tight spot. Slided back to bottom. Reciprocated string and circulated bottom up with sea water at 4600 lpm. Went back to bottom and pumped 20m³ hi-vis pill and displaced well to 1.4 SG mud." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: POOH with 36' BHA from 226m to 150m." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 131m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: At 150m, 5m below sea bed topped up hole with 5m³ 1.4 SG mud. Continued POOH with 36' BHA from 150m to 131m." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 131m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk with night shift prior to POOH with the 36' BHA." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 131m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: General check of handling gear and checked dies in PRS's. Found FWD PRS dies to be normal dies." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 131m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Changed out dies in FWD PRS to Monell dies." "On 2007-11-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: POOH with 36' BHA from 131m to 20m and racked back in derrick." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 36' HO, cleaned and checked HO found in good condition. Laid out 36' HO. Simultaneously ROV/Halliburton prepared forpressure testing of the CRI hose." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed elevators, bails and installed cradles on HTS. Meanwhile operated the CRI valve.Pressure tested the CRI hose to 200bars 10 min, 47l 100bars and 65l 200bars." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Serviced and inspected the TDS." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Isolated and de-isolated TDS." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk prior to rig surface equipment for running conductor. Rigged up same." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk with all involved personnel prior to RIH with 30' conductor" "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 8m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up 30' conductor shoe. Installed 30' bushing and landed conductor in rotary. Filled 30' conductor with water and tested float." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Continued to run in with 30' conductor from 8m to 84m. Tool box talk was held with day shift, prior to running in with 30' conductor." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Held tool box talk prior to change from 30' to 5½' handling equipment. Changed handling equipment" "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up well head housing. Commenced picking up well head housing. Lost communication to auxiliary control." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Re-established communication to auxiliary control." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Picked up and made up the 30' housing. Made up torque is 36 000 ft-lbs (49.000 Nm). Engage locking system with lock-plate. Secure with cap-screws. Inspect housing. Made several attempts to remove the 30' housing protector." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Cut of the protector of the 30' housing." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Broke out housing handling tool. Laid out same. Filled the conductor with sea water to minimize the movement of the conductor." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk prior to handling of the aluminum inner string. Rigged up inner string C-Plate on top of 30' housing joint. Secure plate. Ran aluminum cement stinger. Installed the X-O for the CART." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked the CART from derrick and made up to X-O. Locked CART to housing as per Vetco instruction. Installed inclinometer and handle on 2' fill up valve on CART. Simultaneously rigged up tugger in well bay area for ROV guide lines." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed pull test on CART tool. Removed C-plate. Ran conductor through rotary, and inserted master bushing." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran in with 30' conductor on 5½' HWDP from 84m to 105m. Attached wire sling to conductor housing for pulling arrangement if need it." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued run in with 30' conductor on 5½' HWDP from 105m to 135m, well head level." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Connected up to TDS and filled conductor at 900 lpm, 3,8 bars. Positive indication at shoe." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Ran in with 30' conductor on 5½' HWDP from 135m to 147m. Entered the template." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued RIH with 30' conductor on 5½' HWDP from 147m to 220.8m." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up side entry sub and made up to TDS." "On 2007-11-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Established circulating with 2' valve open at CART tool. Hook load 110 MT. ROV confirmed returns at 2' valve." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Closed 2' valve and established circulation through the 30' shoe." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Verified setting depth with Digiquartz against F-7. Final 110 MT hook load. Checked centralization of conductor housing - OK. Inclination 0.22/0.28 degrees." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Established circulation at 2500 lpm, 3,8 bars, 112 MT hook load. ROV confirmed 2' valve not to be leaking and surveyed for returns, Observed returns from F-5 only. Meanwhile pressure tested cement line to 200 bars 10 min." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Mixed and pumped 55.7 m³ 1.52 sg Tuned Light XL cement slurry at 1100 lpm, 25 bars pump pressure. Confirmed returns to seabed. Displaced cement slurry with 6.7 m³ of SW at max rate using cement unit. FCP 7bars, 600lpm. Bled off pressure, 250 l. Checked for back-flow. Removed cmt hose and flushed through manifolds and hoses." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Waited on cement to set. Meanwhile prepared for wire change on FWD PRS, General maintenance. Started injecting slop into F-12 annulus." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 10.0 hours. Operational details: Waited on cement to set. Meanwhile function tested rotating link adapter and torque wrench. Prepared cantilever for skidding to F-15. Performed general maintenance on the rig floor. Injected slop into F-12 injection annulus." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Confirmed inclinometer before release of CART. Released CART tool. Broke out and laid out the side entry sub and two 5½' pups. Racked back one stand. Dropped one sponge ball and flushed landing string and inner string with sea water. Continued pull out with landing string. With CART in rotary removed 2' valve handle and inclinometer. Function tested CART. Inclinometer measurements CART: Before release, Top: -0.27 Bottom: 0.24 Digiquartz measurement of 30' conductor two measurements after releasing CART: F-5 96584mm F-7 96606mm = F-5 23mm deeper F-5 96603mm F-7 96602mm = F-5 1mm high" "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Broke out X/O and racked back the CART tool in derrick. Laid out the aluminium inner string. Held tool box with night shift prior to handling of the CART tool and aluminium inner string." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.0 hours. Operational details: Prepared for skidding. Meanwhile installed CTS funnel on F-14. Picked up new 36' HO." "On 2007-11-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Held tool box talk prior to skidding of the cantilever from F-5 to F-15" "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.0 hours. Operational details: Removed scaffolding from hatch opening on F-9 and installed hatch covers. Removed hatch cover from F-5. Prepared for skidding." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Held tool box talk prior to skidding rig from F-9 to F-5. Skidded rig 1.5 m port and 2.25 m aft." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Checked that all decks were in alignment. Rearranged hatches on all decks in WH module for F-9 and F-5. Installed scaffolding barriers. Meanwhile transported new 17 1/2' BHA components to drill floor." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: PU and MU 17 1/2' bit, motor, 17 1/4' stab, GWD, power pulse and UBHO. RIH with 17 1/2' BHA to 35 m." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 35m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Checked oil in PRS and serviced same; experienced communication problems to TDS." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 35m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Troubleshot lost communication to TDS. Found faulty profibus connector. MU temporary solution." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 158m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: MU and RIH with 17 1/2' BHA from 35 m to 158 m. Sat UHBO sleeve to high side scribe line. Stabbed into CTS on top of conductor housing while observing with ROV." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Held tool box meeting with both shifts before cutting drill line. Performed cut & slip. Meanwhile changed out faulty profibus connector on top drive." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Continued performing cut & slip. Meanwhile changed out faulty profibus connector on top drive." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 218m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued RIH from 158 m to 195 m. Washed down from 195 m with 2000 lpm / 50 bar / 20 RPM. Tagged cement at 218 m. Connected CTS hose to ROV and started pumping with dredge pump." "On 2007-12-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 220m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Drilled out 30' shoe and rathole from 218 m to 219.5 m MD. Drilling parameters : Flow 3500 lpm / SPP 87 bar / Rotation 40 rpm / Torque 1-3 kNm / WOB 0-3 MT. Reamed back inside shoe for every 2 m drilled. Pumped 10 m3 his-vis sweep as required to clean the hole." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Drilled out 30' shoe and rathole from 217 m to 226 m MD. Drilling parameters : Flow 3500 lpm / SPP 87 bar / Rotation 40 rpm / Torque 1-3 kNm / WOB 1-3 MT. Reamed back inside shoe for every 2 m drilled. Pumped 10 m3 his-vis sweep as required to clean the hole. Reamed hole and shoe track 3 times. No obstruction. Pulled through shoe track with no rotation. No obstruction. Pumped 10 m3 hi-vis and circulated BU while reciprocating 17 1/2' BHA. Up weight 105 MT / down weight 100 MT." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 233m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 17 1/2' section from 226 m to 233 m MD. Drilling parameters : Flow 3100 lpm / SPP 72 bar / WOB 1-3 MT / Torque 1-5 kNm / String RPM 40 / Bit RPM 133. ROP 10 m/hr. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connection. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. Sliding intervals: 230 - 233 m Got good gMWD survey on 215.5 m: Inc 0.18 AZ 182.97. Made two attempts to get gMWD survey at 222.5 m. No sucess." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pulled 17 1/2' BHA back inside shoe at 214 m. Held tool box meeting and RU to run wireline gyro." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: -" "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: POOH single shot gyro from 176 m MD." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 273m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled 17 1/2' section from 233 m to 273 m MD. Drilling parameters : Flow 3000-3400 lpm / SPP 67-88 bar / WOB 2-6 MT / Torque 2-4 kNm / String RPM 40 / Bit RPM 133. ROP 11-20 m/hr. Average ROP 12 m/hr. Pumped 10 m3 hi-vis sweep for every singel drilled. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. Sliding intervals: 230 - 250 m Attempted to get gMWD survey at 261.5 m. No sucess." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 273m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Displaced open hole to 1.40 sg bentonite mud, 10 m3 at 2000 lpm / 55 bar." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: POOH with 17 1/2' drilling BHA from 273 m to 23 m. Stopped with bit inside 30' conductor to inspect TDS and derrick for loose items." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Removed gMWD probe . Lifted probe to drill floor and installed same." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: MU and RIH with 17 1/2' BHA from 23 to 196 m MD." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 273m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued RIH from 196 m to 273 m. Washed down from 196 m with 2000 lpm / 50 bar. Reamed shoe. No obstructions observed. Connected CTS hose to ROV and started pumping with dredge pump." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 280m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 17 1/2' section from 273 m to 280 m MD. Drilling parameters : Flow 3000 lpm / SPP 65 bar / WOB 2 MT / Bit RPM 90. ROP 10 m/hr. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gyro MWD orientation OK. Stopped drilling due to preparations for upcoming ESD test. Sliding intervals: 273 - 280 m" "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 214m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Pumped 10 m3 hi-vis sweep at 280 m to clean the hole. Displaced open hole to 1.40 sg bentonite mud, 15 m3 at 2000 lpm / 55 bar. POOH with 17 1/2' drilling BHA from 280 m to inside 30' conductor shoe at 195 m." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 214m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Performed ESD pre- testing and had power shut down on rig." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 280m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: RIH with 17 1/2' BHA from 195 to 280 m MD. Took survey to link up toolface. Connected CTS hose to ROV and started pumping with dredge pump." "On 2007-12-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 314m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 17 1/2' section from 280 m to 314 m MD. Drilling parameters : Flow 3200 lpm / SPP 74-78 bar / WOB 2-6 MT / Torque 3-4 kNm / String RPM 40 / Bit RPM 136. ROP 15-40 m/hr, average ROP 17 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. Sliding intervals: 280 - 288 m 305 - 314 m" "On 2007-12-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 475m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' section from 314 m to 475 m MD. Drilling parameters : Flow 3200-4000 lpm / SPP 74-160 bar / WOB 3-8 MT / Torque 2-5 kNm / String RPM 40 / Bit RPM 136-160. ROP 40-65 m/hr, average ROP 26.8 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. Sliding intervals: 314 - 328 m 355 - 380 m 395 - 407 m 435 - 447 m" "On 2007-12-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 556m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 17 1/2' section from 475 m to 556 m MD. Drilling parameters : Flow 4000 lpm / SPP 114 bar / WOB 3-4 MT / Torque 2-5 kNm / String RPM 40 / Bit RPM 136-160. ROP +/-35 m/hr, average ROP 18.0 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. Up weight 112 MT / down weight 107 MT. At 556 m made 3 attempts to take gMWD survey. Decided to drill on with MWD inc and azimuth. Sliding intervals: 475 - 487 m 516 - 529 m" "On 2007-12-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 556m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Could not open PS-21 slips due to connection time-out on auxillary SBC computer." "On 2007-12-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 878m. The activity was categorized as 'drilling -- drill' and lasted for 13.0 hours. Operational details: Drilled 17 1/2' section from 556 m to 878 m MD (=Top Utsira). Drilling parameters : Flow 3500-4000 lpm / SPP 114-130 bar / WOB 8-10 MT / Torque 2-3 kNm / String RPM 40 / Bit RPM 105-160. ROP 30-40 m/hr, average ROP 24.8 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed MWD survey on connections. Up weight 120 MT / down weight 112 MT. Sliding intervals: 556 - 571 m 596 - 611 m 636 - 656 m 676 - 696 m 717 - 740 m 756 - 779 m 797 - 817 m 838 - 858 m" "On 2007-12-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1101m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' section from 878 m to 1101 m MD. Base Utsira 1064,5 mMD. Drilling parameters : Flow 3450-4000 lpm / SPP 115-132 bar / WOB 0-12 MT / Torque 4-10 kNm / String RPM 40 / Bit RPM 104-160. ROP 25-100 m/hr, average ROP 37.2 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed gMWD survey on connections. Up weight 138 MT / down weight 118 MT. Sliding intervals: 878 - 888 m 918 - 928 m 958 - 973 m 999 - 1019 m 1039 - 1065 m 1079 - 1101 m" "On 2007-12-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1415m. The activity was categorized as 'drilling -- drill' and lasted for 12.0 hours. Operational details: Drilled 17 1/2' section from 1101 m to 1415 m MD. Top Skade 1225 mMD. Base Skade 1316 mMD. Drilling parameters : Flow 3500-4130 lpm / SPP 106-148 bar / WOB 1-10 MT / Torque 6-13 kNm / ECD 1.01 - 1.09 SG/ String RPM 40/Bit RPM 136-160. ROP 1-100 m/hr, average ROP 26.2 m/ hrs. Pumped 10 m3 hi-vis sweep for every single drilled. Performed gMWD survey on connections. Up weight 149 MT / down weight 123 MT. Max ECD in Skade 1.09 SG Survey. Inc. Azi. 1131.84 18.41 118.87 1164.55 21.19 116.01 1171.98 22.67 114.88 1212.44 26.61 110.18 1252.67 30.29 110.42 1293.19 29.76 111.71 1333.68 28.07 113.27" "On 2007-12-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1414m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: At TD. Pumped 30 m³ Hi-vis followed by 30 m³ sea water, followed by another 30 m³ of Hi-vis, at 3500 lpm while reciprocating drill string." "On 2007-12-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1414m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Displaced out pill with sea water 1 x BU, 3500 lpm 110 bars. Reciprocating the string." "On 2007-12-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1414m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Displaced hole to 1.40 SG at 3500-4500 lpm, SPP 170-230 bars." "On 2007-12-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1123m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: POOH with 17½' BHA from 1415 m to 1123 m. Took weight of 20 MT overpull. RIH with two jnts. POOH with rotation on the string, passed obstruction with 5 MT overpull." "On 2007-12-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 720m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued POOH with 17½' BHA from 1123 m to 720 m. Tight spots at 796 m and 775 m, pulled through with 10 -15 MT overpull." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued POOH with 17½' BHA from 720 m to 122 m. Tight spots at 519 m and 481 m, pulled through with 10 -15 MT overpull." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Removed PS-21 slip and installed master bushing. Held tool box take prior to handling the 17½' BHA." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up to TDS and displaced string to sea water." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued POOH BHA from 122 m to 35 m." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Prepared for racking back the UBHO." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Racked back the 17½' BHA." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and cleared the rig floor." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to rig up 13 3/8' casing handling equipment." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Rigged down the 5½' handling equipment. Rigged up the 13 3/8' casing handling equipment and FAC tool and function tested same. Meanwhile moved the CTS funnel from F-5 to F-15." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to run in hole with 13 3/8' casing." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up shoe, intermediate and float collar and Baker locked same. Confirmed float OK." "On 2007-12-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 819m. The activity was categorized as 'drilling -- casing' and lasted for 10.8 hours. Operational details: RIH with 13 3/8' casing from 27 m to 819 m, filling every casing joint." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Continued RIH with 13 3/8' casing from 819 m to 1250 m, filling every casing joint." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to change surface handling equipment and picking up the 18 3/4' Well Head." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Changing to 5½' handling equipment." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rigged up 5½' handling equipment." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up CART." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 18 3/4' WH housing/CART assembly. Made up to 13 3/8' casing." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rigged down casing tong and PS-30 13 3/8' slips. Cleared rig floor." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1270m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lowered CART below rotary, removed cap and filled up CART with sea water." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1270m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk prior to install the master bushing, and installed same." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1405m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 5½' HWDP landing string as per tally, picked up 2 x HWDP and cement head and made up same. Installed Lo-torque valve and cement hose. Up/down weight 180/125 MT. Landed 18 3/4' WH into 30' conductor by setting down casing string weight, plus 5 MT of landed string weight and engaged the lock ring. Performed over pull test to 25 MT." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1405m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Established circulation in steps with SW through top drive to 2300 lpm 21 bars." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1405m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Confirmed line up and leak tested line up to 200 bars 5 min." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1405m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Mixed and pumped 161 m³ 1.52 sg lead at 1300 lpm / 24 bar followed by 20 m³ 1.92 sg tail slurry at 900 lpm / 34 bar. ROV observed returns only came up F-5. Displaced and sheared wiper plug by pumping 3000 litres SW, plug sheared at pressure/volume: 132 bar/ 1200 ltr. Continued to displace cement with seawater at 3000 l/min using mud pumps. FCP 90 bars, bumped plug and applied 160 bars to plug. Pump efficiency : 95.4 %. Bled off pressure, 1500 litres bled back to the cement unit. Disconnected cement hose after pressure had been bled off." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1405m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Reduced overpull on landing string to neutral. ROV observed CART. Released CART according to Vetco, 5 turns right hand." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box talk prior to lay out cement head. Removed cement hose and Lo-torque valve, broke out cement head. Dropped 2 sponge balls and flushed landing string." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with landing string and racked back same. Laid out CART." "On 2007-12-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Installed hatch covers on wellhead and moon pool. CONTINUED OPERATIONS ON WELL F-15 Y1" "On 2008-07-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.8 hours. Operational details: Cleaned and cleared rig floor of WL equipment. Held tool box meeting prior to skidding the cantiliver from F-14 to F-5. Prepared to skid rig. Started to skid rig to F-5. Meanwhile RU to pump through KWV on F-14." "On 2008-07-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Continued skidding cantiliver from F-14 to F-5. Meanwhile performed line test against KWV on F-14 30/345 bar 5/10 min. Equalized and opened HMV and DHSV by pressuring up to 67 bar using baseoil and cmt unit according to F-14 initial start up procedure." "On 2008-07-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Continued skidding cantiliver from F-14 to F-5. Had rig shut-down." "On 2008-07-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Changed burst disk in turbine cooling system and rectified problem. Re-sat all rig systems." "On 2008-07-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Continued skidding cantiliver from F-14 to F-5." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Continued skidding cantiliver from F-14 to F-5. Skidded 3 m port and 2.25 m aft." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed master bushings and installed safety guard. RU to install riser spider." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Equalized and opened HMV and DHSV by pressuring up to 63 bar using baseoil and cmt unit to start up on F-14 after shut-down." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Continued to install riser spider. Function tested riser spider and installed hole cover. Installed and function tested BX-elevator." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box meeting prior to lifting TBC riser joint to drill floor. Installed Vetco equipment on rig floor. Lifted riser simultaniously with crane and TDS until it was vertical. Removed slings." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed protection from connector. Prepared to bring Vetco hot stabs from moonpool to rig floor to be able to function test TBC." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Flushed and function tested TBC. Meanwhile removed cradle and trolly from HTS. Removed special tool and dressed fox hole for MU 12 1/4' BHA." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.0 hours. Operational details: Waited on production to bean up F-14. Meanwhile: - lifted tension cylinders for F-9 to rig floor and placed them next to riser spider for easy acess when lifting them down to WH. - pressure tested standpipe manifolds - PU and MU drill collars from deck." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: Waited on production to stop production on F-14 and F-12 for heavy lift. Meanwhile continued PU and MU drill collars from deck and pressure testing standpipe manifolds." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Removed hatches on F-5 and F-10. Lowered tension cylinders for F-9 through rotary down to WH and retrieved actuator for F-14." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Removed tension deck hatches from F-5 and F-10. RU guide line tuggers in moonpool. Meanwhile re-instated cradle and trolly to HTS for riser handling." "On 2008-07-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Held tool box talk with night crew. PU and ran HPDR doubles from surface to 50 m. Removed lifting sub on HPDR in riser spider and MU flange connection. Installed protection caps on flange nuts using Bandak tool. Tested flanges to 3000 psi/5 min. Installed fairings around flanges. Verified that tension ring was in place on top of the centralizer deck opening. Meanwhile installed guide wires at template using ROV." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Continued to PU and run HPDR doubles from 50 to 103 m. Removed lifting sub on HPDR in riser spider and MU flange connection. Installed protection caps on flange nuts using Bandak tool. Tested flanges to 3000 psi/5 min. Installed fairings around flanges. Meanwhile leak tested kill manifold 30/345 bar for 5/10 min and choke/kill manifold 30/345 bar for 5/10 min." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 127m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Continued to MU flange connection. Installed protection caps on flange nuts using Bandak tool. Tested flanges to 3000 psi/5 min. Installed fairings around flanges. PU riser string using TDS and RD riser spider. Lowered HPDR so that Claxton tool was below rotary and installed outer ring and master bushings. PU and MU one std of 5 1/2' DP." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: RIH with HPDR from 127 m to just over connector at 138 m. Entered guide funnel. Removed guide funnel from well head. Turned riser clockwise until hot stab was oriented in the right direction. Landed TBC on WH with 15 MT. Launched hot stab and locked connector onto WH. Applied 10 MT overpull on riser to confirm H4-MUSL connector." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Installed centralisers, tension ring and boat collison stool. Meanwhile performed line test on kill line to F-12 to 30/200 bar for 5/10 min. Equalized and opened F-12 DHSV." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Retrieved hot stab on TBC and replaced with dummy. Retrieved guide wires from template." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Re-installed hatch on F-10." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Attempted to install half-moon hatches on F-5 around BOP joint. Removed master bushings and retracted blocks to line up hatches without sucess." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Rig shut down due to production. Meanwhile held tool box talk prior to pressuring up tension cylinders." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Waited for production operator to transfer weight from HPDR to tension cylinders. Meanwhile carried out housekeeping on centralizer deck." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Released tension on TDS and adjusted pressure on tension cylinders to 37 bar." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Installed half-moon hatch cover on F-5. Erected 3 m scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap. Meanwhile pressured up to 90 bars on all 4 tension cylinders to obtain riser tension of 150 MT. Held tool box talk prior to equalizing DHSV on F-14." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Continued to erect scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap. Meanwhile equalized and opened DHSV by pressuring up to 88 bar using baseoil and cmt unit to start up production on F-14." "On 2008-07-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued to erect scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued to erect scaffolding tower around Claxton tool in moonpool to be able to insert Veco 1502 Male cap." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Filled riser with 8.7 m3 SW and installed Veco 1502 Male cap." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: RU and performed integrity test of riser system through TDS and Claxton tool using cmt unit. Leak tested HPDR/well to 20/195 bar for 5/10 min. Ok. Pumped 1275 ltrs at 700 lpm and bled back 1200 ltrs." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Disconnected Claxton tool. Could not RB std of 5 1/2' DP due to PRS not working. Meanwhile carried out maintenance on FWD iron-roughneck and prepared 12 1/4' BHA." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Re-sat AFT PRS after shut-down." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RB std of 5 1/2' DP and removed Claxton tool from rig floor. Re-installed master bushings." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box talk prior to nipple up BOP/diverter. Moved BOP to top of HPDR and started to nipple up BOP. Meanwhile pressure tested 5 1/2' TIW and grey valve to 30/345 bar for 5/10 min." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.8 hours. Operational details: Held tool box talk prior to nipple up BOP and focused on tools aloft. Moved BOP to top of HPDR and started to nipple up BOP onto NT2 connector. Installed slick joint." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Installed overshot and diverter. POOH and LO diverter RT. Removed diverter inserts and installed outer ring and master bushings. Cleared rig floor of excess equipment. Meanwhile flogged bolts on slick joint." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Filled riser with SW using cmt unit and held tool box talk prior to MU test plug assembly. Had problem with BX-elevators." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: BX-elevator would not close. Changed out rental elevators for rig elevators." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: Checked dies on PRS prior to PU 5 1/2' DP. PU and MU BOP test plug assembly. RIH with BOP test plug on 5 1/2' DP from surface to 139.4 m." "On 2008-07-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.5 hours. Operational details: Lined up and pressure tested NT2 connector / riser to 30/345 bar for 5/10 min. Ok. Lined up and pressure tested lower IBOP, upper IBOP and kelly hose to 30/345 bar for 5/10 min. Ok. Performed accumulator test. Meanwhile serviced both FWD and AFT PRS. Serviced and inspected TDS." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.2 hours. Operational details: RD and LO BOP test plug assembly. Function tested shear rams and recorded parameters. Meanwhile cleaned and cleared drill floor." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 92m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Held tool box talk with focus on manual handling of BHA. PU and MU 12 1/4' BHA from surface to 92 m." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 92m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Rig shut down. Waiting on production to free electrican to re-set drill floor equipment." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 92m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waiting on production to free electrican to re-set drill floor equipment." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Held tool box talk with focus on manual handling of BHA. PU and MU 12 1/4' BHA from 92 m to 140 m." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to equalizing and opening HMV on F-14." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 987m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 140 m to 180 m. Broke off liner XO on btm of 5 1/2' DP std. Removed master bushings and installed PS21 slips. Continued to RIH with 12 1/4' BHA on 5 1/2' DP from 180 m to 987 m filling every 10 stds. Meanwhile equalized and opened HMV on F-14." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 987m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: MU TDS and tested MWD tools at 2400 lpm / 48 bar. Removed PS21 slips and installed master bushings. Installed TIW." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 987m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Performed slip and cut." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 987m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Continued to perform slip and cut." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Removed TIW and master bushings. Installed PS21 slips. RIH with 12 1/4' BHA on 5 1/2' DP from 987 m to 1307 m." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: MU TDS and performed choke drill. Operation transfered to F-99." "On 2008-07-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Perform choke drill." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1376m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued to RIH with 12 1/4' BHA on 5 1/2' DP from 1307 m to 1351 m. Down weight 108 MT. Held tool box talk prior to displacing well to 1.35 sg OBM. Made up TDS and broke circulation. Washed down from 1351 m at 2300 lpm / SPP 43 bar and tagged cement plug at 1376,5 m MD." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1376m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Drilled on cement plug/float at 1376,5 m MD and displaced to 1.35 sg OBM. Drilling parameters : Flow 2800 lpm / SPP 114 bar / String RPM 20-30 / WOB 4-5 MT / Torque 8-10 kNm / ECD 1.36. Picked off bottom every 10-15 min to clean bit. Meanwhile MU and RB 10 3/4' csg. stds." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1376m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Drilled on cement plug/float at 1376,5 m MD. Drilling parameters : Flow 2800 lpm / SPP 114 bar / String RPM 20-30 / WOB 5-10 MT / Torque 8-12 kNm / ECD 1.36. Picked off bottom every 10-15 min to clean bit. Meanwhile MU and RB 10 3/4' csg. stds. A total of 3 stds 10 3/4' csg RB in derrick." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1376m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Drilled on cement plug/float at 1376,5 m MD. Drilling parameters : Flow 2800 lpm / SPP 111 bar / String RPM 40-70 / WOB 1-11 MT / Torque 2-20 kNm / ECD 1.36 sg EMW. Picked off bottom every 10-15 min to clean bit. Meanwhile MU and RB 10 3/4' csg. stds." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1415m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Drilled out shoe track from 1376.5 m to 1415 m MD. Drilling parameters : Flow 2800 lpm / SPP 112 bar / String RPM 70 / WOB 2-6 MT / Torque 9-20 kNm / ECD 1.36 sg EMW. Reamed through shoe every 2 m drilled. Meanwhile MU and RB 10 3/4' csg. stds." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1418m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 3 m new formation in 12 1/4' hole section from 1415 m to 1418 m MD. Drilling parameters : Flow 2800 lpm / SPP 112 bar / String RPM 70 / WOB 2 MT / Torque 9-10 kNm / ECD 1.36 sg EMW. Meanwhile MU and RB 10 3/4' csg. stds." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1415m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.8 hours. Operational details: Spotted 5 m3 LCM pill in open hole/TD; Flow 2800 lpm / SPP 112 bar / String RPM 10 / Torque 9 kNm. Reduced flow to 1600 lpm going through MWD tools. Circulated and POOH until bit just below 13 3/8' csg shoe; Flow 2800 lpm / SPP 112 bar / String RPM 10 / Torque 9 kNm. Meanwhile held toolbox prior to performing FIT and MU and RB 10 3/4' csg. stds." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1415m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: Closed BOP and lined up to perform FIT. Performed line test to 100 bar / 5 min against IBOP and Kill HCR. Performed FIT and pressured up at 50 lpm to 33 bar (36 bar on cmt unit) using 298 ltrs SW. Bled back 230 ltrs. Meanwhile MU and RB 10 3/4' csg. stds." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1415m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Filled trip tanks with 1.35 sg OBM and displaced choke and kill manifolds to mud. Meanwhile MU and RB 10 3/4' csg. stds. A total of 12 stds 10 3/4' csg RB in derrick." "On 2008-07-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1522m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Established parameteres and started drilling 12 1/4' hole section from 1418 m to 1522 m MD. Drilling parameters : Flow 3250-3300 lpm / SPP 153-159 bar / String RPM 120 / WOB 2-4 MT / Torque 11-15 kNm / ECD 1.37 sg EMW / ROP 30-50 m/hr. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1653m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole section from 1522 m to 1653 m MD. Drilling parameters : Flow 3300-3500 lpm / SPP 159-179 bar / String RPM 120 / WOB 2-4 MT / Torque 13-17 kNm / ECD 1.37-1.38 sg EMW / Drilled with limited ROP 20-40 m/hr due to problems transfering slurry from milling tank through active tank to holding tank. Meanwhile MU and RB 9 5/8' csg. stds. A total of 14 stds 9 5/8' csg RB in derrick." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1672m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 12 1/4' hole section from 1653 m to 1672 m MD. Drilling parameters : Flow 3500 lpm / SPP 179 bar / String RPM 120 / WOB 2-4 MT / Torque 13-17 kNm / ECD 1.38 sg EMW / Drilled with limited ROP 20-40 m/hr due to problems transfering slurry from milling tank through active tank to holding tank. Stopped drilling to investigate TDS. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1672m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Investigated leak in TDS. Found small leak on lower side of washpipe. Decided to continue operation and keep observing TDS. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1793m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled 12 1/4' hole section from 1672 m to 1793 m MD. Drilling parameters : Flow 3500 lpm / SPP 172-174 bar / String RPM 120-150 / WOB 3-4 MT / Torque 12-19 kNm / ECD 1.37-1.38 sg EMW. Unable to drill on because holding tank was full (unable to inject slurry because it did not meet viscosity requirement) and cuttings screw going to skip clogged up. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1793m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Circulated while reciprocating drill string; Circulation parameters : Flow 2800 lpm / SPP 117 bar / String RPM 50 / Torque 8-12 kNm / ECD 1.36 sg EMW due to problems with mill pump and slurry system. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1862m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 12 1/4' hole section from 1793 m to 1862 m MD. Drilling parameters : Flow 3500 lpm / SPP 176 bar / String RPM 150 / WOB 3-6 MT / Torque 12-20 kNm / ECD 1.38 sg EMW. Unable to drill on due to line from shaker to mill tank, line from mill tank to active tank and cuttings screw going to skip clogged up. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1862m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Circulated while reciprocating drill string; Circulation parameters : Flow 1000-2000 lpm / SPP 22-30 bar / String RPM 50 / Torque 5-9 kNm / ECD 1.37 sg EMW due to problems with mill pump and slurry system. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1886m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 12 1/4' hole section from 1862 m to 1886 m MD. Drilling parameters : Flow 3500 lpm / SPP 184 bar / String RPM 150 / WOB 1-3 MT / Torque 9-17 kNm / ECD 1.38 sg EMW. Drilled with limited ROP 20 m/hr to observe proper operation of mill pump and slurry system. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1895m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 12 1/4' hole section from 1886 m to 1895 m MD. Drilling parameters : Flow 3500 lpm / SPP 184 bar / String RPM 150 / WOB 2-3 MT / Torque 14-20 kNm / ECD 1.37 sg EMW. Drilled with limited ROP 20 m/hr to observe proper operation of mill pump and slurry system. Stopped drilling due to exhaust fumes on drillfloor. RU cascade system on drill floor. Meanwhile shut down csg. equipment. A total of 29 stds 9 5/8' csg RB in derrick." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1383m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held tool box talk regarding, CRI & slurry system, servicing the TDS and start to RIH with drilling BHA and continue drilling 12¼' hole." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1383m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Serviced the TDS." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1383m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Checked surface equipment prior to RIH with drilling BHA." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1876m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: RIH from 1383m to 1551m. Performed kick drill 29 sec. Continued RIH from 1551m to 1876m." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1895m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made up to TDS and filled the pipe. Performed survey at 1876m. Washed down and tagged bottom at 1895m." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1955m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled 12¼' hole section from 1895 m to 1955 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / String RPM 150 / WOB 2-5 MT / Torque 9-21 kNm / ECD 1.37-1.38 sg EMW / ROP 25-40 m/hour Problems pumping slurry from active tank to Slurry holding tank due to high viscosity. Simultaneously MU and RB 9 5/8' csg. stds." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1955m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Racked back one stand and circulated at reduced rate 30 rpm, 50 rpm, 1100 lpm. Due to cuttings ditch to holding tank blocked." "On 2008-07-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1979m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Contined drilling 12¼' hole section from 1955 m to 1979 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / String RPM 150 / WOB 4-7 MT / Torque 8-22 kNm / ECD 1.37-1.38 sg EMW / ROP 25-35 m/hour Simultaneously MU and RB 9 5/8' csg. stds." "On 2008-07-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2145m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Contined drilling 12¼' hole section from 1979 m to 2145 m MD. Drilling parameters : Flow 3500 lpm / SPP 180 bar / String RPM 150 / WOB 2-11 MT / Torque 10-22 kNm / ECD 1.37-1.395 sg EMW / ROP 30-45 m/hour. At 2000m started to increase the mud weigth. Took survey after every connection. Simultaneously MU and RB 9 5/8' csg. stds. Total in derrick 36 stds." "On 2008-07-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2405m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: Continued drilling 12¼' hole section from 2145 m to 2405 m MD. Drilling parameters : Flow 3500 lpm / SPP 190 bar / String RPM 150 / WOB 2-8 MT / Torque 14-21 kNm / ECD 1.462-1.465 sg EMW / ROP 5-46 m/hour. Took survey after every connection. Simultaneously MU and RB 9 5/8' csg. stds." "On 2008-07-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2399m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: BHA torqued up and stalled out. Released torque and pulled with 50 MT overpull. Attempted to free pipe by rotation. No indication that hole had packed off. Had full circulation. Fired jars two times and came free. Established rotation at full circulation 3500 lpm, to circulate clean the BHA. Experienced sticky tendencies when going down to 2402m." "On 2008-07-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2399m. The activity was categorized as 'drilling -- ream' and lasted for 2.0 hours. Operational details: Racked back one stand and reamed one stand at 3500 lpm 140 rpm up and 40 rpm down." "On 2008-07-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2480m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Continued drilling 12¼' hole section from 2405 m to 2480 m MD. Drilling parameters : Flow 3500 lpm / SPP 202 bar / String RPM 150 / WOB 2-4 MT / Torque 18-22 kNm / ECD 1.459-1.465 sg EMW / ROP 15-31 m/hour. Took survey after every connection Simultaneously MU and RB 9 5/8' csg. stds." "On 2008-07-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 12¼' hole section from 2480 m to 2601 m MD. Drilling parameters : Flow 3500 lpm / SPP 202 bar / String RPM 150 / WOB 4-9 MT / Torque 15-28 kNm / ECD 1.456-1.459 sg EMW / ROP 20-30 m/hour. Took survey after every connection Stringer at 2518m - 2523.5m MD and 2587m - 2588 m MD. Simultaneously MU and RB 9 5/8' csg. stds. Total in derrick 50 stds." "On 2008-07-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2641m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued drilling 12¼' hole section from 2601 m to 2641 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 150 / WOB 3-8 MT / Torque 20-28 kNm / ECD 1.457-1.461 sg EMW / ROP 19-32 m/hour Simultaneously MU and RB 9 5/8' csg. stds. Geoservices unit shut down." "On 2008-07-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2641m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Picked up and circulated and reciprocated the string. Geo-services unit did shut down due to air tight door was not shut probably. Geo-services purged and re-booted the unit." "On 2008-07-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2860m. The activity was categorized as 'drilling -- drill' and lasted for 12.2 hours. Operational details: Continued drilling 12¼' hole section from 2641 m to 2860 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 160 / WOB 2-4 MT / Torque 18-31 kNm / ECD 1.458-1.463 sg EMW / ROP 20-40 m/hour. Geo-Services unit was down until 11:30. Observed gas level manually in unit. Took survey after every connecting Lost power to both mud pumps. Picked off bottom. Simultaneously MU and RB 9 5/8' csg. stds." "On 2008-07-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2860m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Due to generator tripped in process module, power supply was cut out to both mud pumps. Generator back on line and both mud pumps up running." "On 2008-07-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2898m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drilling 12¼' hole section from 2860 m to 2898 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 160 / WOB 3-8 MT / Torque 23-35 kNm / ECD 1.462-1.463 sg EMW / ROP 6-35 m/hour." "On 2008-07-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2900m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Tagged hard formation at 2898m MD. Continued drilling 12¼' hole section from 2898 m to 2900 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 80 / WOB 10 MT / Torque 23-35 kNm / ECD 1.462-1.463 sg EMW / ROP 1-4 m/hour." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2918m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 12¼' hole section from 2900 m to 2918 m MD. Drilling parameters : Flow 3500 lpm / SPP 210 bar / String RPM 160 / WOB 8-10 MT / Torque 12-35 kNm / ECD 1.445-1.450 sg EMW / ROP .5-5 m/hour." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2927m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Continued drilling 12¼' hole section from 2918 m to 2927 m MD. Drilling parameters : Flow 3500 lpm / SPP 217 bars / String RPM 160 / WOB 3-8 MT / Torque 14-35 kNm / ECD 1.445-1.451 sg EMW / ROP 1-4 m/hour." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2922m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated well clean while reciprocating the string. 3500 lpm 220 bars." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2878m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Pulled one stand wet." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2878m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Dropped the Gyro at 1300 hours. Made up to TDS and rotated the string at 10 rpm." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2878m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well, well static. Meanwhile held tool box talk prior to POOH with 12¼' drilling BHA. Installed wiper rubber, checked dies in PS 21 slips." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2722m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 12¼' drilling BHA wet from 2927m to 2722 m. Oberved no drag." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2722m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well, well static." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1391m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: Made up TDS and pumped 5m³ 1.65 SG slug. Continued POOH with 12¼' drilling BHA from 2722m to 1391m inside the shoe. Oberved no drag." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1391m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well, well static." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 526m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Continued POOH with 12¼' drilling BHA from 1391m to 526 m." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 526m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed kick drill. Informed drill crew about the use of escape mask." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued POOH with 12¼' drilling BHA from 526m to 135m." "On 2008-07-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: Laid out 12¼' drilling BHA." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued laying out 12¼' drilling BHA, Bit and Powerdrive." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleared and cleaned drill floor." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk and picked up and made up jet sub and wear bushing RT. Stopped operations due to exhaust fumes on drill floor. Waiting time recorded on F-99." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Held tool box talk and continued making up wear bushing RT. RIH and retrieved the wear bushing at 139 m. Washed the WH. POOH with wear bushing." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to service TDS, derrick inspection and change dies in AFT PRS." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Laid out the wear bushing and the RT." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Performed derrick inspection." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Serviced the TDS and inspected for loose items." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Changed dies in AFT PRS and inspected rollers in AFT and FWD PRS's." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed 5½' elevators and bails from the rig floor." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Made up FAC tool to TDS. Installed casing bails." "On 2008-07-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rigged up casing elevator." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Function tested casing elevator." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Rigged up casing tong. Retrieved master bushing and installed automatic casing slips." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH with 9 5/8' casing and change out dies in FWD PRS." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Changed dies in FWD PRS." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up the shoe and checked the integrity. Picked up Intermediate jnt., Float jnt. and Baker locked the Shoe track." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1010m. The activity was categorized as 'drilling -- casing' and lasted for 6.2 hours. Operational details: RIH with 9 5/8' casing from 38m to 1010m. Filled every stand with FAC tool. Broke circulation 550 lpm 23 bars." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1397m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued RIH with 9 5/8' casing from 1010m to shoe at 1397m. Filled every stand with FAC tool. Broke circulation 550 lpm 25 bars." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1994m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Continued RIH with 9 5/8' casing from 1397m to 1994m. Filled every stand with FAC tool. Broke circulation 550 lpm 27 bars." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2305m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued RIH with 9 5/8' casing from 1994m to 2305m. Filled every stand with FAC tool. Took weight." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2305m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Worked string up/down free." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2305m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Held tool box talk and changed out inserts of Odfjel elevator from 9 5/8' to 10 3/4'." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2305m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and made up X-O 9 5/8' x 10 3/4'." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2305m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk and changed out inserts in of FMS slip and in the casing tong from 9 5/8' to 10 3/4'." "On 2008-07-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2608m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Continued RIH with 10 3/4' casing from 2323m to 2608m. Filled every stand with FAC tool." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2778m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued RIH with 10 3/4' casing from 2608m to 2778m. Filled every stand with FAC tool." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2778m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rigged down Odfjel elevator, FAC tool and long bails. Counted casing on cantilever and back-up sub's." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2778m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up and rigged up drilling bails and 5½' elevators." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2778m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and made up 10 3/4' casing hanger / PADPRT assy." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2785m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged down Odfjel slip and extension ring. Installed master bushing." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2785m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged down Odfjel casing tong." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2861m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 10 3/4' x 9 5/8' csg on 5 1/2' HWDP landing string from 2785m to 2861m MD. Filled every stand." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2916m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 10 3/4' x 9 5/8' csg on 5½' HWDP landing string. P/U M/U cement head to top drive." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2916m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Broke circ & picked up in stage to 2000 LPM, 77 bars, took losses, reduced to 1000 LPM - loss free rate. Total lost 11m³." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Landed off csg as per Vetco procedure." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Picked up pumps to 1000 LPM & Circ one casing volume 5800 stks pumped. Simultaneously held tool box talk prior cmt job." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped 8 m³ base oil from pit 14, 1000 LPM. Pump 20 m³ spacer 1.50 SG from pit 12, 1000 LPM." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced spacer in surface lines with 3m³ OBM & closed IBOP. Opened Lo-torq valve on cmt head and dropped 1 3/4' ball." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Mixed and pumped 17.3 m³ 1.90 SG cement according to Halliburton procedure. Bottom plug sheared at 80 bars." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced cmt to rig floor with 500 liters water, released dart and continued pumping 2500 liter water behind cement, dart sheared top wiper plug @ 205 bars." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Displaced cmt with rig pumps 1000 LPM, at 2700 stk lost suction to MP changed from pit #7 to pit # 9 losses approx. 3 m³. Increased rate to 1500 LPM at 3200 stks. At 4082 stks btm plug sheared @ 135 bars. FCP 43 bars @ 1000 LPM, bumped plug at 4909 stks final pressure 113 bars. 96% pump efficiency." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressure tested casing to 345 bars 15 min." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Checked for back flow, float holding. Disconnected cmt hoses and flushed lines." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rotated 4 turns to right to engage MS1 Seal. Engaged and set MS1 seal as per Vetco procedure, 35 bars/207 bars 10 min." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Leak tested MS1 seal 35/345bars 5/10 min." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released PADPRT, 4 turns to right" "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: L/O cmt head" "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Dropped Halliburton sponge balls 2 ea and flush string using mud 1770 lpm. POOH PADPRT." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Out of hole with PADPRT inspected same. Laid out same." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: MU Wear Bushing RT, RIH and installed wear bushing according to Vetco procedures." "On 2008-07-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Commenced BOP test." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 6.0 hours. Operational details: Continued performing BOP test. Simultaneously cleaned out filters on mud pumps and cleaned out mill tank." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.8 hours. Operational details: Continued test BOP 25/345bar 5/10 min, as per MCN test procedure." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleared & cleaned around RT." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 5m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Released wear bushing RT. POOH wear bushing RT from 138m to 5m, strapped pipe. Measured Datum 138,87m." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk and laid out wear bushing." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared & cleaned around RT." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk prior to M/U 8½' BHA." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: M/U 8½' BHA from surface to 61m." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk and installed radioactive source." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued M/U 8½' BHA from 61m to 70m." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed to 5' handling equipment & checked PRS dies." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued M/U 8½' BHA from 70m to 90m." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 116m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Dressed auto slips to 5'." "On 2008-07-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1216m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: RIH with 8½' BHA on 5' DP from 116m to 1216m. Tested MWD tools at 484m. Filled the pipe every 500m." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1339m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Continued RIH with 8½' BHA on 5' DP from 1216m to 1339m." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1339m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Made up 5' x 5½' XO. Changed to 5½' DP handling equipment." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1502m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued RIH with 8½' BHA on 5½' DP from 1339m to 1502m. Observed problem with TDS control software. Parallel activity: Started injecting slops into F-14 annulus." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1502m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Electrician investigated, and rectified the error on TDS." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2551m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued RIH with 8½' BHA on 5½' DP from 1502m to 2551. Filled the pipe every 500m." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2551m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Commenced changing out the Wash pipe on the TDS." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2551m. The activity was categorized as 'interruption -- maintain' and lasted for 1.8 hours. Operational details: Continued changing out the Wash pipe on the TDS. Held 15 min handover crew change." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2551m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Made up to TDS. Filled pipe & established circulation prior to perform choke drill. Simultaneously serviced TDS." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2551m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed choke drill." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2874m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Held tool box talk and RIH 8½' BHA from 2551m to 2874m." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2892m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Established circulation 1600 lpm & washed down from 2874m to 2892m." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2894m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Tagged TOC at 2892m, Drilled out float from 2893m to 2894m. Drilling parameters: Flow 1600 lpm / SPP 128 bar / String RPM 40 / TQ 16-19 kNm. Simultaneously displaced well to 1,30 SG OBM." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2921m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Drilled out shoe track from 2894m to 2921m. Drilling parameters: Flow 1600 lpm / SPP 140 bar / String RPM 40 / TQ 14-17 kNm. MUD weight 1.30 SG. Reamed the shoe and pulled back through shoe with no rotation." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2927m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Cleaned out rat hole in 1-2 m intervals from 2921m to 2927m. Experienced pack off and TDS stalled, 2nd time as reaming into shoe with bit at shoe. Also saw pack off with bit on bottom, stopped pumping slump pipe opposite direction of movement, No losses seen after pack off." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2930m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled new formation from 2927m to 2930m. Cleaned out rate hole and verified no restrictions. Drilling parameters: Flow 1600 lpm / SPP 130 bar / String RPM 160 / WOB 1-3 MT / TQ 17-20 kNm. MUD weight 1.30 SG." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2930m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Observed 120 litres gain in trip tank." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2913m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Racked back one stand. Observed the well on trip tank, well static." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2913m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Rigged up pump in sub and surface lines for FIT test." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2913m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Took FIT equivalent to 1.65 SG, using 1.30 SG OBM. Pumped 80 lpm and applied 92 bars to the string and annulus. Shut down the pump. Downhole reading from Schlumberger equivalent to 1,658 SG." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2913m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.2 hours. Operational details: Rigged down pump in sub and surface lines. Lined up for drilling." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2913m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Took survey at 2913m and set tool" "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2945m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued to drill 8½' hole from 2930m to 2945m. Drilling parameters: Flow 2100 lpm / SPP 214 bars / String RPM 100 Bit 260 / WOB 8-13 MT / TQ 15-20 kNm / ROP 8 m/hour / ESD 1.393 SG / MUD weight 1.30 SG. Observed active pit did not drop as drilling ahead." "On 2008-07-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2945m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Picked up and took flow check on the trip tank, well static." "On 2008-07-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2994m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Continued to drill 8½' hole from 2945m to 2994m. Drilling parameters: Flow 2100 lpm / SPP 214-240 bars / String RPM 100-120 Bit 260-280 / WOB 8-13 MT / TQ 15-20 kNm / ROP 8-20 m/hour / ESD 1.379-1.393 SG / MUD weight 1.30 SG. Problems operating the AFT PRS. Took survey after every connection." "On 2008-07-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2994m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Electrician investigated the error. Found that the pipe size setting of the AFT PRS was incorrect. As investigating the error of the AFT PRS. Reciprocated the string one jnt circulating 2100 lpm 206 bars. Meanwhile switch to the FWD PRS and picked up 5½' DP." "On 2008-07-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3000m. The activity was categorized as 'drilling -- survey' and lasted for 1.8 hours. Operational details: Continued to drill 8½' hole from 2994m to 3000m. Drilling parameters: Flow 2100 lpm / SPP 214-240 bars / String RPM 100-120 Bit 260-280 / WOB 8-13 MT / TQ 19-21 kNm / ROP 4 m/hour / ESD 1.393-1.401 SG / Increased MUD weight from 1.30 SG to 1.35 SG. Took survey after connection. Had to down link twices det proper Power setting from 50 to 35. Down linked Xceed to get tool face setting from 288 to 268." "On 2008-07-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3155m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued to drill 8½' hole from 3000m to 3155m. Drilling parameters: Flow 2100 lpm / SPP 240 bars / String RPM 130 Bit 290 / WOB 8-13 MT / TQ 16-30 kNm / ROP 40-50m/hour / ECD 1.419-1.569 SG / MUD weight 1.35-1.45 SG. Took survey after every connection. Reamed one single prior to connection." "On 2008-07-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3233m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Continued to drill 8½' hole from 3155m to 3233m. Drilling parameters: Flow 2100 lpm / SPP 240-250 bars / String RPM 100-130 Bit 260-290 / WOB 6-11 MT / TQ 16-30 kNm / ROP 2-50m/hour / ECD 1.536-1.570 SG / MUD weight 1.45 SG. Reamed one single prior to connection when high ROP.Took survey after every connection. Problems with CRI transfer pump on the active tank. Parallel operation: Made up 7' liner in stands and racked back in derrick." "On 2008-07-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3233m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Found the housing of the CRI transfer pump washed out. Installed new housing. Meanwhile lined up to be able to operate the CRI system manually." "On 2008-07-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3260m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Continued to drill 8½' hole from 3233m to 3260m. Drilling parameters: Flow 2100 lpm / SPP 240-250 bars / String RPM 130-150 Bit 290-310 / WOB 6-16 MT / TQ 21-25 kNm / ROP 5-15m/hour / ECD 1.569-1.571 SG / MUD weight 1.45 SG. Took survey after connection. Down linked tool. Cleaned in lower shaker. Parallel operation: Made up 7' liner in stands and racked back in derrick" "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3292m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Continued to drill 8½' hole from 3260m to 3293m. Drilling parameters: Flow 2100 lpm / SPP 240-260 bars / String RPM 130-150 Bit 290-310 / WOB 4-6 MT / TQ 22-27 kNm / ROP 7-25m/hour / ECD 1.569-1.582 SG / MUD weight 1.45 SG. Took survey after connection. Down linked tool. Poor response from Xceed. Parallel operation: Made up 7' liner in stands and racked back in derrick." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3280m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Poor response from Xceed. Unable to keep well path. Discussed situation with Geologist in town and concluded to POOH and change BHA." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3240m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Pulled back one stand and circulated well clean and 2100 lpm 230 bars. Reciprocated the string. Parallel operation: Made up 7' liner in stands and racked back in derrick. Total in derrick 9 stds." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3240m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well, well static." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3157m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Commenced to POOH with 8½' BHA wet." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3157m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: M/U TDS and down linked the LWD tools." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3157m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Lined up to trip tank & flow checked well on trip tank, well static." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3157m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 10 m3 slug 1.65 SG." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued POOH with 8½' BHA from 3157m to 2914m, no restrictions seen when pulling into shoe." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2914m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well on trip tank, well static. Meanwhile service TDS." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1340m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Continued POOH with 8½' BHA from 2914m to 1340m on 5½' DP. Trip time 700 m/hour." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1340m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed to 5' handling gear." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Continued POOH with 8½' BHA from 1340m to 140m on 5' DP. Trip time 600 m/hour." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well, well static. Meanwhile held tool box talk prior to L/O BHA." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned around rotary table." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Changed to master bushing & checked PRS dies." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 8 1/2' BHA from 140m to 61m." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed radioactive source from BHA." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Continued L/O BHA from 61m to surface." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Inspected bit & Xceed tool, decided to run back-up bit." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk and checked equipment." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Laid out Xceed and BHA components." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Picked up and made up new 8½' BHA. RIH from surface to 42m." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk and erected barriers prior to handling radio active source." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pulled BHA back to Ecoscope and inserted radioactive source. Ran back in to 42m." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed out handling gear from 5½' to 5'." "On 2008-07-27, at Well NO 15/9-F-5, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Continued RIH with 8½'BHA from derrick 5' HWDP from 42m to 99m. Checked Totco ring." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Installed autoslips." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 303m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued RIH with 8½ BHA on 5' DP from 99m to 303m. Filled string every 300m. Trip time 407 m/hour." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 303m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Filled string, empty trip tank. Made up x-over to string and test MWD tools, 1600 lpm. Good. Removed x-over." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1320m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Continued RIH with 8½ BHA on 5' DP from 303 to 1320m. Filled string every 300m. Monitored displacement on trip tank. Trip time 407 m/hour." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1320m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Installed 5' x 5½' XO. Changed handling equipment to 5½'." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1844m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued RIH with 8½ BHA on 5½' DP from 1320 to 1844m. Filled string every 300m. Monitored displacement on trip tank. Trip time 524 m/hour." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2651m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: RIH with 8½ BHA on 5½' DP from 1844 to 2651m. Filled string every 300m. Monitored displacement on trip tank. Trip time 323 m/hour" "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2651m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Serviced FWD PRS, due to unexplained noise." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2920m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 8½ BHA on 5½' DP from 2651 to 2920m. Filled string every 300m. Monitored displacement on trip tank. Trip time 359 m/hour" "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3259m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Broke circulation at shoe and washed down from 2920m to 3259m." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3259m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued RIH with 8½ BHA on 5½' DP from 2920 to 3259m. Filled string every 300m. Monitored displacement on trip tank." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3294m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Took connection and made up to TDS. Reamed from 3259m to 3294m and took survey with bit at 3293m." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3293m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Tight hole after survey. Pulled with 40 MT overpull. Attempted to slump down pipe with rotation. Jared up with 240 MT and freed pipe. Established and rotation reamed slowly up." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3294m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Reamed full stand from 3259m to 3294m." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3283m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took survey @ 3283m, good survey." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3367m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Continued to drill 8½' hole from 3292m to 3367m. Reamed Draupne transition zone from 3338m to 3300m. Drilling parameters: Flow 2100 lpm / SPP 210 bars / String RPM 130-180 / WOB 6-11 MT / TQ 24-38 kNm / ROP 17-40 m/hour / ECD 1.586-1.601 SG / MUD weight 1.45 SG. Took survey after every connection. Down linked tool. Parallel operation: Made up 7' liner in stands and racked back in derrick." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3367m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Unexplained gain approx 300ltr. Spaced out & observed well on trip tank." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3366m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Took SCRs as per below table @ 3366m." "On 2008-07-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3500m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Continued to drill 8½' hole from 3367m to 3500m. Reamed Draupne transition zone from 3419m to 3388m. Drilling parameters: Flow 2100 lpm / SPP 205-209 bars / String RPM 180 / WOB 3-8 MT / TQ 20-26 kNm / ROP 30-50 m/hour / ECD 1.602-1.619 SG / MUD weight 1.45 SG. Took survey after every connection. Down linked tool. Parallel operation: Made up 7' liner in stands and racked back in derrick." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Continued to drill 8½' hole from 3500m to 3580m. Drilling parameters: Flow 2100 lpm / SPP 205-209 bars / String RPM 180 / WOB 3-6 MT / TQ 26-28 kNm / ROP 30-50 m/hour / ECD 1.582-1.604 SG / MUD weight 1.45 SG. Took survey after every connection. Down linked tool. Held tool box talk as drilling ahead prior taking pressure points. Parallel operation: Made up 7' liner in stands and racked back in derrick." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3566m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Evaluated where to take pressure points. Down linked the StethoScop. Meanwhile reamed single between 3580 and 3566m in preparation for taking pressure point. 2100 lpm, 80 to 120 rpm. Downlinked to set tool (Stethoscope) to standby." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3566m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Send down link to set tool and took pressure point reading: Bit depth 3565.5m, test depth 3530m." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3600m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued to drill 8½' hole from 3580m to 3600m. Drilling parameters: Flow 2100 lpm / SPP 210 bars / String RPM 180 / WOB 5 MT / TQ 26-28 kNm / ROP 16-42 m/hour / ECD 1.594 SG / MUD weight 1.45 SG. Took survey after connection. Parallel operation: Made up 7' liner in stands and racked back in derrick. Total 27 stds in derrick." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3620m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued to drill 8½' hole from 3600m to 3620m. Drilling parameters: Flow 2100 lpm / SPP 212 bars / String RPM 130-180 / WOB 5-11 MT / TQ 25-30 kNm / ROP 40-50 m/hour / ECD 1.584-1.601 SG / MUD weight 1.45 SG. Took survey after connection. Down linked tool. Stringer uncounted at 3593m" "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3586m. The activity was categorized as 'drilling -- survey' and lasted for 1.2 hours. Operational details: Send down link to set tool and took pressure point reading: Bit depth 3585.9m, test depth 3551m." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3661m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued to drill 8½' hole from 3620m to 3661m. Drilling parameters: Flow 2100 lpm / SPP 212 bars / String RPM 130 / WOB 5-11 MT / TQ 25-30 kNm / ROP 40-50 m/hour / ECD 1.584-1.601 SG / MUD weight 1.45 SG. Took survey after connection. Down linked tool." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3661m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Unexplained gain. Lined up on trip tank & observed well, well static" "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3649m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Send down link to set tool and took pressure point reading: Bit depth 3648.9m, test depth 3624m." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3742m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Continued to drill 8½' hole from 3661m to 3742m. Drilling parameters: Flow 2100 lpm / SPP 206 bars / String RPM 130 / WOB 4-11 MT / TQ 19-30 kNm / ROP 4-40 m/hour / ECD 1.585-1.612 SG / MUD weight 1.45 SG. Took survey after every connection. Down linked tool. Slow drilling from 3712,8m to 3720m." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3742m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: Send down link to set tool and took pressure point reading: Bit depth 3730.9m, test depth 3706m. Bit depth 3720.9m, test depth 3696m." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Continued to drill 8½' hole from 3742m to 3792m. Drilling parameters: Flow 2100 lpm / SPP 206 bars / String RPM 130 / WOB 4-11 MT / TQ 19-30 kNm / ROP 4-40 m/hour / ECD 1.585-1.612 SG / MUD weight 1.45 SG. Took survey after connection. Down linked tool." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Circulated cuttings clear of BHA, racked back one stand." "On 2008-07-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3783m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Circulated well clean while reciprocating the string. Circulation parameter: Flow 2100 lpm / SPP 190 bars / String RPM 120 / MUD weight 1.45 SG. Curculated a total of 3 buttoms up." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3783m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Continued circulated well clean while reciprocating the string. Circulation parameter: Flow 2100 lpm / SPP 190 bars / String RPM 120 / MUD weight 1.45 SG." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well, well static." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3541m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH wet with 8½' BHA from 3792m to 3700m." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3700m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: Send down link to set tool and took pressure point reading: Bit depth 3694m, test depth 3660m. Bit depth 3677m, test depth 3643m. Were not able to achieve a good test in stead of StethoScope did not performed which could be interpreted as failure." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH wet with 8½' BHA from 3700m to 3580m." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- survey' and lasted for 1.8 hours. Operational details: Send down link to set tool and took pressure point reading: Bit depth 3556m, test depth 3522m. Were not able to achieve a good test in stead of StethoScope did not performed which could be interpreted as failure." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3460m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Flow checked well, well static. Pumped 1.65 SG slug 5m³." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2813m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH with 8½' BHA from 3460m to 2813m." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2813m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Took foot print prior to run 7' liner." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2813m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Observed well on trip tank. Meanwhile serviced TDS and checked dies in PRS." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2530m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH wet with 8½' BHA form 2813m to 2530m. Trip time 1132 m/hour." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2530m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 1.65 SG slug 5m³." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1320m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH wet with 8½' BHA form 2530m to 1320m. Trip time 807 m/hour." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1320m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Changed to 5' handling equipment." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH wet with 8½' BHA form 1320m to 221m. Trip time 628 m/hour." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well prior to pull the BHA. Erected barriers prior to handling radioactive source." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pulled the last 3 stds 5' DP from 221m to 99m. Removed auto slips. Removed Totco ring and drift from top single of HWDP." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk prior to POOH with BHA and lay out same.." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: POOH and laid out 8½' BHA. Found damaged StethoScope seals." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Rigged up from running 7' liner." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH with 7' liner." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and made up shoe track. Checked the integrity of the shoe." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- wait' and lasted for 0.2 hours. Operational details: Waited on crane due to helicopter." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up float jt & landing collar jt. RIH from 10m to 37m." "On 2008-07-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued RIH 7' liner in stands from 37m to 130m. Filled every 2'ed stds.Trip time 186 m/hour (15.5 jnt/hour)" "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 355m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued RIH 7' liner in stands from 130m to 355m. Filled every 2'ed stds.Trip time 150 m/hour (12.5 jnt/hour)" "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 364m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Installed pup jts & PIP tag from 355m to 364m" "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 863m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Continued RIH 7' liner in stands from 364m to 863m. Filled every 2'ed stds. Trip time 222 m/hour (18.5 jnt/hour)" "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 863m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk and re-arranged 7' liner stds FWD in set back area. To be able to reach with AFT PRS." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 969m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued RIH 7' liner in stands from 863m to 969m. Filled every 2'ed stds. Trip time 212 m/hour. (17.5 jnt/hour)" "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 969m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk and picked up 7' liner hanger." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 969m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up liner hanger assy to 7' liner." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 969m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox handover meeting." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 980m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed masterbushing and bowls. Installed RA marker in pup joint below hanger. Ran Liner hanger assy through rotary. Checked shear pins on hanger." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 988m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Filled PBR with drillwater." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 988m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged down Odfjell tong and FMS. Changed eleavator inserts from 5' to 5 1/2'." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 988m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made up TDS and filled string with OBM from active." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 988m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk. Removed masterbshing and intalled automatic slips in rotary." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran 7' liner / liner hanger on 5 1/2' DP from 988 m to 1082 m MD. Picked up singles from cantilever (7 ea)." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2899m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Ran 7' liner / liner hanger on 5 1/2' DP from 1082 m to 2899 m MD." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2899m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke circulation at 9 5/8' casing shoe. Circulated 1 x liner volume (~20 m3) at 1150 lpm / 55 bar SPP. Took up/down weights 162/126 MT." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3746m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Ran 7' liner / liner hanger on 5 1/2 DP from 2899 m to 3746 m MD." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3787m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up TDS and washed down 7' liner from 3746 m to 3787 m MD at 500 lpm / 42 bar SPP. Meanwhile made up and tested cement hose to cement head laying on the HTS." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3787m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up cement head with 6 m pup to string. Made up TDS to cement head. Took up/down weights 200/137 MT." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3793m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH while circulating at 500 lpm and tagged TD at 3793,3 m with 10 MT." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up ~1 m and to located liner hanger at setting depth. Increased rate in increments to 1000 lpm / SPP 76 bar. Set torque limit to 34 kNm. Commenced rotation and increased rotation in increments to 20 rpm. Rotating torque 23-26 kNm." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Dropped liner hanger setting ball and chased same with 500 lpm." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Observed pressure build up when setting ball seated after 712 strokes. Pressured up to 160 bar to set liner hanger and maintainted pressure for 2 min. Verified hanger set by slacking off weight to 105 MT (30 MT applied) - ok. Bled off stand pipe pressure. Released liner hanger running tool with 12 clockwise rotations. Took up/down weights 155/123 MT - running tool free." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Sheared ball seat by applying pressure on DP. Ballseat sheared out at 251 bar." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Stepped up rate in 500 lpm increments to check for stable returns / loss free rate. 500 lpm / 38 bar SPP. 1000 lpm / 66 bar SPP. 1500 lpm / 110 bar SPP. No losses observed." "On 2008-07-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Decreasead rate to 1000 lpm and started rotating at 20 rpm. Torque 12-16 kNm. Increased rate to 1500 lpm and cirucalted bottoms up while rotating at 20 rpm. Meanwhile held prejob meeting prior to cementing." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated bottoms up at 1500 lpm while rotating string at 20 rpm." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped 8 m3 baseoil followed by 15 m3 tuned spacer E+ and 3 m3 baseoil. Pumprate 1000-1500 lpm. Rotated string at 20 rpm. Released lower DP dart." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up cement unit. Mixed and pumped 21,6 m3 1,90 sg cement at 840 lpm. Pump pressure 60-100 bar. Displaced cement with 890 litres of drillwater and closed lo-torque to cement head. Released upper DP dart." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Displaced cement with 1,45 sg OBM using rig pumps. Pump rate 1200-1600 lpm. Observed shear of lower wiper plug at 432 strokes pumped, sheared out at 230 bar pressure. Observed bottom wiper plug in landing collar at 1254 strokes, sheared out at 74 bar. Observed no shear/pressure peak when upper dart landed in upper wiper plug. Observed pressure bulid up from 5 bar to 136 bar when cement entered annulus after ~1300 strokes. Reduced rate to 500 lpm after 2130 strokes. Bumped plug after 2228 strokes with 190 bar (FCP ~100 bar). Pump effciency 97,8%. No losses observed during displacement." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Bled off pressure on standpipe to ~5 bar. Pressure increased to 16 bar in 10 min. Lined up to trip tank and observed for backflow. Observed ~50 liter increase in 20 min. Broke off cement hose on drillflloor and drained to trip tank. Observed flow from hose after draining cement head. Took 3 consecutive measurements on back flow rate - 33 sec/l - 37 sec/l - 40 sec/l - rate steadily decreasing - ok." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up string to engage TSP packer actutating dogs. Set down 30 MT to set TSP packer. Observed dual shear - ok." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3792m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up cement unit to BOP kill inlet. Closed BOP. Pressure tested TSP packer to 280 bar / 10 min. Pressure drop 1,8 bar (0,64%) with improving trend." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2820m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated out excess cement." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2820m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated out excess cement at 2000 lpm." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2820m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Ran liner hanger running tool back into PBR to position coupling for breaking out cement head." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2820m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for laying out cement head." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2812m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Disconnected lo-torques, cement hose and hydraulic control lines from cement head. Broke and laid out cement head with 6 m DP pup." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2785m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Inserted sponge balls. Made up TDS and pulled free of PBR with liner hanger running tool. Circulated 1,5 x string volume at 2000 lpm / SPP 68 bar to clean DP." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: POOH with liner hanger running tool on 5 1/2' DP from 2785 m to 121 m MD. Tripping speed 888 m/hrs." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Function tested BOP. Meanwhile held toolbox talk for breaking cement head." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up cement head with 6 m pup from HTS and made up same to string to ease breaking out pup joint. Broke off 6 m pup joint. Laid out cement head." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with liner hanger running tool on 5 1/2' DP from 121 m to 27 m MD. Laid out 7 x ea 5 1/2' DP singles." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Took time out for safety meeting adressing forthcomming operations with manrider." "On 2008-08-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed automatic slips. Pulled liner hanger running tool through rotary. Reset tool according to Weatherford instructions. Laid out and inspected tool - ok. ****Operations transferred to F-99*****" "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up well protector assy and hung off same in rotary. RIH with well protector on 5 1/2' DP to 170 m MD. Made up magnet / 11' jet-sub assy." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH and Jetted accross BOP with 1500 lpm / 10 bar SPP." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Spaced out and located jet sub underneath BOP. Functioned BOP pipe rams and annular." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Reciprocated string and made 3 passes across BOP with jet sub." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 310m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH on 5 1/2' DP from 190 m to 310 m MD. Made up TDS to each stand. Washed drilling riser with 1800-3000 lpm while running in." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with wellprotector / jet sub on 5 1/2' DP from 310 m MD to surface. Laid out jet sub and well protector. Recovered approx 300 g swarf and cuttings in well protector (1-5 cm)." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Rigged up for running 3 1/2' DP. Changed dies in IR. Changed inserts in DP elevator. Prepared PS-21 slips. Lifted cleaning assy #1 and #2 onto HTS." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 12m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Changed dies in IR. Cleared and tidied drillfloor. Picked up and hung off cleaning assy #1 - 6' PDC bit and pup in manual slips. Picked up and made up cleaning assy #2 - 7' razor back / well sweep magnets." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 12m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held toolbox / handover meeting." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 12m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Reconfigured HTS rollers on cantilever. Removed masterbushing and installed PS-21 slips in rotary." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 559m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.2 hours. Operational details: Picked up 3 1/2' singles from deck and RIH with cleaning assemblies from 12 m to 559 m MD. Observed that a 3 1/2' DP single was caught by the PDM and dislogded on the HTS rolles." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 559m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Took time out for safety. Investigated situation. Probable cause was that the pipe was staggered relative to the rest when being picked up, or that it had bounced off the rollers when the PDM grip was released." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 910m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Continued picking up 3 1/2' singles and RIH with cleaning assemblies from 559 m to 910 m MD." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 910m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held toolbox talk. Changed from 3 1/2' to 5 1/2' handing equipment. Changed die-holders and dies in IR. Placed cleaning assy #3 - top-dress/polish mill / well commissioner / 9 5/8' razor back / wellsweep magnets, on HTS." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 950m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Picked up and made up celaning assembly #3. Picked up and made up cleaning assembly #4 - MFCT / well patroller / wellsweep magnets." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 991m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Made up stand of 5 1/2' DP. Made up TDS. Broke circulation and stepped up pumps to 1000 lpm / 88 bar SPP. Took up/down weights 82/85 MT." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 991m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to slip and cut drill line." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 991m. The activity was categorized as 'interruption -- maintain' and lasted for 4.0 hours. Operational details: Hung off travelling block. Slipped and cut drill line according to Mærsk procedure. Meanwhile worked on AFT PRS." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 991m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Picked up travelling block." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 991m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Calibrated travelling block." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1554m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: RIH with cleaning assemblies on 5 1/2' DP from 991 m to 1554 m MD. Meanwhile rigged up casing tong for doing paralell operations." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1584m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Scraped and cleaned VBM plug setting depth in 9 5/8' casing at 640 m MD +/- 15 m. Made 2 passes with scrapers circulating at 1900 lpm / SPP 270 bar. Observed hydraulic leakaged from elevator." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1594m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Not able to access leakage point. Changed DP elevator." "On 2008-08-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1748m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with cleaning assemblies on 5 1/2' DP from 1594 m to 1748 m MD." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2804m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: RIH with cleaning assemblies on 5 1/2' DP from 1748 m to 2804 m MD." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2804m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Took up/down weights 147/121 MT. Free rotating weight 132 MT. Free rotating torque at 20 rpm was 9 kNm. Circulated 50 m3 OBM at 1900 lpm / 285 bar to condition mud." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2815m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Entered PBR with 6' bit while rotating 20 rpm and circulating at 500 lpm / SPP 37 bar. No obstruction observed." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2868m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with cleaning assemblies on 5 1/2' DP from 2815 m to 2868 m MD." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2868m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Elevator not functioning correctly on given commands. Changed back to original elevator which had been fixed." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3131m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued to RIH with cleaning assemblies on 5 1/2' DP from 2868 m to 3131 m MD." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3170m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up and made up 2 x 5 1/2' DP singles. Picked up and made up cleaning assy #5 - 10 3/4' razor back / posi drift / well sweep magnets / well patroller." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3654m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: RIH with cleaning assemblies on 5 1/2' DP from 3170 m MD to 3654 m MD." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3668m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Picked up 5 1/2' singel. Took weight at 3656 m MT. Scraped cement from 3656 m to 3668 m MD. Parameters : Flow 1640 lpm / 270 bar SPP / 50 rpm / torque 15 kNm." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3708m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Picked up full stand of 5 1/2' to scrape cement. Scraped cement from 3668 m MD to 3708. Parameters : Flow 1640 lpm / 260 bar SPP / 50 rpm / torque 15 kNm." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3708m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Set back stand and replaced with 3 x 5 1/2' singles picked up from deck. Ran back to 3708 m MD." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3735m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Scraped cement from 3708 m to 3735 m MD. Parameters : Flow 1640 lpm / 256 bar SPP / 50 rpm / torque 15 kNm." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Entered PBR while rotatiing 40 rpm and circulating at 1000 lpm. TOL tagged at 2809,5 m MD. Dressed off PBR with 30 rpm, torqued up to 17 kNm." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3727m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked up to place polish mill ~5 m above PBR. Circulated 2,5 x liner volume at 1800 lpm / SPP 295 bar / 60 rpm." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Entered PBR while rotating 30 rpm. Sheared MFCT open by setting down 30 MT." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated 1.5 x well volume above TOL at 4000 lpm / SPP 270 bar / 60 rpm / torque 10 kNm." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cycled MFCT to closed position according to SPS instructions. Confirmed closed MFCT by pumping 1600 lpm / SPP 230 bar - ok." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set well commissioner packer by setting down 20 MT. Closed MPR. Tested packer to 70 bar-using rig pumps - ok." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3735m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up weight to unset packer. Pumped 1640 lpm / SPP 230 bar to confirm MFCT still closed." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3735m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Displaced choke and kill line to base oil through standpipe #1." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pumped 33,9 m3 base oil through one standpipe and down the DP at 340 lpm. Circulated welll on trip tank to confirm stable. U-tube pressure 153 bar before setting well commissioner." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Set well commissioner by setting down 20 MT. Lined up to cement unit and bled off well in stages to 12 bar. Bled back 750 liter." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3733m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Inflow tested well. Pressure rose 6,6 bar in 30 min. Bled down pressure again and held test for another 45 min, test levelled out towards end, dropped 0,2 bar last 10 min. Equalised well commissioner by pressuring up to 153 bar. Picked up 7 m and unset well commissioner packer." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3732m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Displaced lines and manifolds to seawater using cement unit. Filled soap in trip tanks." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3732m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held tolbox meeting prior to pumping displacement train." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3732m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pumped well cleaning fluids : 10 m3 dope cleaning pill, 30 m3 hi-vis push pill, 15 m3 hi-vis soap pill, 10 m3 hi-vis soap pill, 10 m3 seawater and 15 m3 hi-vis soap pill. Routed OBM returns to pits. Pump rate 1500-3000 lpm / SPP 270-290 bar. Rotated at 50 rpm and reciporcated string while pumping. Observed torque values up to 27 kNm when baseoil travelled up annulus." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3733m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Reset stroke counter. Pumped 20 m3 seawater, 20 m3 packer fluid and 31 m3 seawater to place the packer fluid in the 7' liner. Pump rate 2600-3500 lpm / SPP 270-290 bar." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3733m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Ran in while rotating and opened MFCT / set well commissioner by setting down 20 MT on the liner top." "On 2008-08-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Maintained 20 MT on MFCT / well commisioner and continued pumping. Pumped seawater at 3100-4000 lpm / SPP 80-130 bar / 60 rpm." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pumped seawater at 3100-4000 lpm / SPP 80-130 bar / 60 rpm. Took consecutive NTU readings on seawater returns: 398/317/224/166/411/580/491/799/1000+/780. Pumped a total of 180 m3 seawater." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3739m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Stopped rotation. Pumped packer fluid at 3800 lpm / SPP 118 bar. Took consecutive NTU reading on packer fluid returns: 106/89/80/121/250/130/111/115/125/115. Pumped a total of 270 m3 packer fluid." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3733m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up to unset well commissioner and operated MFCT to closed position. Spaced out and closed MPR. Lined up cement unit." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3733m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pressure tested casing/liner to 345 bar / 10 min. Observed 0,5 bar drop / 10 min (0,15%) towards end of test - ok. Pumped and bled back 2280 liter." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3733m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flowchecked well on trip tanks - well static. Meanwhile terminated building 7' tubing stands and prepared for laying out singles / pulling DP." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3647m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Broke out and set back 5 1/2' DP stand. Pulled, broke and laid out 4 x 5 1/2' DP singles." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3170m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: POOH with cleaning assemblies on 5 1/2' DP from 3647 m to 3170 m MD." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3749m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Broke out an laid down cleaning assy #5 - 10 3 /4' razor back / posi drift / wellsweep magnets / well patroller." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3011m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke and laid out 2 x 5 1/2' DP singles. POOH with cleaning assemblies on 5 1/2' DP from 3131 m to 3011 m MD." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2201m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: POOH with cleaning assemblies on 5 1/2' DP from 3011 m to 2201 m MD. Got problems with HPU indicating hydraulic leakage." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2201m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Troubleshot HPU. Found leakage on hose to PS-21 slips. Removed slips. Installed masterbushing to continue pulling pipe using manual slips." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2000m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: POOH with cleaning assemblies on 5 1/2 DP from 2201 to 2000 m MD. Used manual slips." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2000m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed masterbushing. Installed PS-21 automatic slips and function tested same." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 950m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: POOH with cleaning assemblies on 5 1/2' DP from 2000 m to 950 m MD." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 920m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Broke out and laid out cleaning assy#4 - MFCT / well patroller / wellsweep magnet and cleaning assy #3 - polish/top-dress mill / well commissioner / wellsweep magnets. Recovered 4 kg swarf on magnets. Nothing recovered in well patrollers." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 920m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Set up AFT PRS for racking 3 1/2' DP stands. Not able to rack stands using AFT PRS." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 920m. The activity was categorized as 'interruption -- other' and lasted for 7.0 hours. Operational details: Troubleshot racking problem. Calibrated fwd PRS. Attempted to rack pipe with FWD PRS - negative. Calibrated AFT PRS, not able to rack pipe. Had problems with anti-collission system and pipe clashed with racking fingers. Fixed hydraulic leakge on HPU which may have caused malfunction on anti-collision system. Had problems with 'pipe set down' function, system not registering when pipe set down. Parked AFT PRS. Continued to troubleshot FWD PRS. Attempted to rack stand of pipe - ok." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 30m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: POOH with cleaning assemblies on 3 1/2' DP from 920 m to 30 m MD. Racked back 3 1/2' DP in foldable fingerboard using FWD PRS. Removed automatic slips and installed masterbushings." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pulled and laid out 2 x 3 1/2' DP singles. Broke and laid out cleaning assy #2 - 7' razor back / wellsweep magnets. Broke and laid out cleaning assy #1 - 6 ' PDC bit." "On 2008-08-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment. Lifted VMB plug onto HTS." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and hung off VMB plug / setting tool in rotary." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 608m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with VBM plug / setting tool on 5 1/2' DP from surface to 608 m MD." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 638m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH on last stand to 638 m MD while circualting packer fluid at 800 lpm / SPP 2 bar. Stopped pumping. Took up/down weights 95/89 MT." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 638m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rotated pipe clockwise at 15 rpm and slacked off weight. Stopped rotation and set down to 60 MT. Took 30 MT overpull to confirm plug set. Confirmed plug set with packer element at 636,5 m MD and top of plug at 634 m MD." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 638m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set down to 87 m MT in block. Made 3 attempts to shear sleeve for closing ball vavle (3/4, 1,5 and 2 lefthand turns)- nogo. On 4th attempt the shear sleeve sheared out just after 2 turn and 3100 Nm applied torque. Pressured up to 30 bar on string above plug. Rotated string righthand to re-open ball valve and observed pressure dropping to 16 bar." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 638m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up cement unit. Pressured up to 280 bar, observed losing ~10 MT weight on plug. Picked up weight to 82 MT on block. Continued pressuring up to 380 bar, observed losing ~4 MT on plug. Held test for 20 min, last 10 min 0,5 bar drop (0,13%). Pumped and bled back 1880/1800 liter." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 638m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rotated DP lefthand to close ball valve. Applied 30 bar on DP to check that ball valve closed." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 633m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 5 m to get free of plug. Spotted 5 m3 hi-vis pill on top of plug at 1500 lpm / SPP 4 bar. Chased hi-vis with packer fluid." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with VMB plug setting tool on 5 1/2' DP from 628 m to 130 m MD." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed PS-30 slips. Installed masterbushing." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: POOH with VMB plug setting tool on 5 1/2' HWDP from 130 m MD to surface." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Laid down VMB plug setting tool. Prepared WBRRT for retrieveing wearbushing. Held toolbox talk and handover meeting. Meanwhile closed shear ram and lined up cement unit to pump down kill line. Pressure tested VMB plug from above to 345 bar / 10 min (0,2% drop)." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Reset WBRRT according to Vetco instructions. RIH to 140 m MD on 5 1/2' DP and engaged tool. Pulled free wearbushing with 34 MT overpull." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with WBRRT and wear bushing." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Released and laid out wearbushing. Reset WBRRT according to Vetco instructions. Laid down WBRRT." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up jetting sub to stand of 5 1/2' HWDP. RIH on 2 x stands of 5 1/2' HWDP to 115 m MD." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 254m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Made up PADPRT to 18 3/4' lock down sub. Landed PADPRT on 10 3/4' casing hanger at 139 m MD. Set down 7 MT on PADPRT and rotated 4 1/4' turns to initiate locking sequence." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 254m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed line test from cement unit to kill lline HCR. 35/345 bar 5/10 min - ok. Closed LPR." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 254m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Made 4 attempts to set lock down sub by pressuring up between LPR and PADPRT. Observed too high volumes pumped and no pressure building up. Repeated setting procedure 3 times but obtained same negative result." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with PADPRT and lockdown sub from 139 m MD to surface. Inspected lockdown sub and found score marks indicating junk preventing proper landing. Broke out and set back PADPRT." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up stand. Made up TDS and RIH with jet sub to +/- 140 m MD. Made 3 passes and jetted across wellhead at 4100 lpm / SPP 65 bar. Pumped a total of 45 m3 packer fluid." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 254m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Racked back stand used for jetting. Picked up and made up PADPRT. RIH on 5 1/2' HWDP and landed PADPRT at 139 m MD. Rotated string and set down weight as instructed by Vetco." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 254m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Closed LPR and lined up from cement unit to pump in BOP kill line. Pressurised above PADPRT in 35 bar increments up to 207 bar to set lock down sub - ok." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Disengaged from lock down sub. POOH on 5 1/2' HWDP from surface. Laid out PADRT tool and jet sub." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran in with stand of 5 1/2' DP. Closed annular. Purged air in kill line in atttempt to empty riser and BOP. POOH with stand of DP. The BOP was accidentally left closed when pulling.stand, weight came up rapidly and the last tooljoint slipped through the annular causing a shock." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Inspected drill line and crown block for damage - none found." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared and tidied drillfloor before removing diverter." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed elevator and installed sling for pulling diverter. Remove master bushing and outer ring." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled diverter and set back on drillfloor." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Attached sling to diverter slick joint, pulled and laid out slickjoint." "On 2008-08-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Rigged down slings. Installed outer ring, masterbushing and hole cover." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Removed BOP tension cylinders. Nippled down BOP. Removed/rebuilt scaffolding. Moved BOP to starboard setback area in moonpool. Meanwhile made up PR tension joint handling flange to stand of DP. Ran guidewire for hotstab. ROV engaged hotstab in TBC receptacle." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox / short change handover meeting." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up claxton tool. Removed outer ring and master bushing and ran claxton tool through RT. Installed outer ring and master bushing. Hung off claxton tool on pup joint. Made up 5 1/2' DP stand, ran in and landed Claxton tool on top of HPDR BOP joint." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Made up studs on claxton tool to 4500 Nm using Hy-torq tool and torque plate." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared tools and equipment from scaffolding in moonpool." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Took 5 MT overpull on riser. Bled down pressure on tension cylinders and transferred tenison to block until 60 MT in block. Meanwhile brought riser spider to drillfoor and function tested same." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Ran cylinders and lowered tensioner assembly. Disconnected tension cylinders and pulled aside. Dismanteled tensioner assembly. Dismanteled contact ring. Hoisted up contact ring. Removed centralizer and boat collision stool. Lowered tension ring onto the protector guide." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to unlacthing TBC. Confirmed injection well F-4 shut down for heavylift operation." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Pressured up through minireel/hotstab to 3000 psi to unlock the TBC connector." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed hotstab in TBC connector and installed dummy stab using ROV." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lifted off TBC connector and came free from wellhead in on continuos stroke. Pulled claxton tool / HPDR to just under rotary table for setting slips. Set slips. Broke out and set back 5 1/2' DP stand." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held toolbox talk for installing riser spider." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed master bushing and outer ring. Pulled 1st HPDR double - BOP joint and tension joint - through rotary. Installed riser spider in well center. Hung off HPDR in riser spider." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Removed fairings. Broke connection using bolt tensioner tools. Laid out 1st double with simulatneous lift by deck crane and TDS. Installed handling flange type C on 2nd double - upper pup joint and splash zone joint." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 77m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with HPDR to 77 m. Removed fairings. Hung off HPDR in riser spider." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 77m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Broke connection using bolt tensioner tools. 2 bolt tensioner tools got jammed on bolts. Meanwhile installed VX ring, guide funnel and hole cover on F-5 subsea wellhead." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 77m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Freed bolt tensioner tools that jammed/malfunctioned. Traced back up tools." "On 2008-08-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 77m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Continued breaking connection using bolt tensioner tools. Installed handling flange type C on 3rd double - std joint#4 and std joint#5." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 77m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Laid out 2nd double with simultaneous lift by deck crane and TDS" "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with HPDR double to 49 m. Removed fairings. Hung off HPDR in riser spider." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Broke connection using bolt tensioner tools. Installed handling flange type C on 4th double - std joint#2 and lower pup joint." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with HPDR to 24 m. Checked zink anodes. Checked inside TBC for VX ring - none. Removed fairings. Hung off HPDR in riser spider." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Broke connection using bolt tensioner tools. Installed handling flange type C on 5th double - std joint#1, lower pup joint and TBC. Meanwhile removed tension ring 002 and installed tension ring for PR riser (10008802) on Centralizer deck." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Laid out 4th double with simultaneous lift by deck crane and TDS." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting prior to laying out 5th double." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH 5th double - std joint #1, lower pup and TBC to surface. Laid out 5th double with simultaneous lift by deck crane and TDS." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleaned and tided drillfloor." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk for transfering F-5 production coflex hose to XMT deck." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Transferred production coflex hose from drillfloor to XMT deck using tuggers." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk for picking up production riser and re-arranging hatches in wellherad module." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed hatches on slot F-10. Re-arranged/built scaffolding barriers around F-5 and F-10. Configured riser spider for running production riser." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up 1st joint - TBC and stress joint, with simultaneous lift by deck crane and TDS. Chekcked / re-arranged guidwire clamp." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: RIH with TBC stress joint and hung off in riser spider. Picked up 1st double - lower pup joint and std joint #1 with simulatneous lift by deck crane and TDS. Removed handling flange on 1 st joint. Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings. Attached guidewire slings and fore-runner on TBC / stress joint." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: RIH with production riser to 20 m. Function trested TBC and performed pre-operational checks according to Vetco procedure." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH with production riser to put guidewire clamp in convenient working height at Centealizer deck. Caught guidewires and attached to ROV hooks/slings on guidewire clamp. Ran guidewires indivdually to 2 m above riser guide funnel at seabed. RIH to 37 m and hung off production riser in riser spider." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up 2nd double - 2 ea standard joints with simulatneous lift by deck crane and TDS. Removed handling tool type E from 1st double." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH with production riser to 66 m. Hung off production riser in riser spider. Removed handling flange type E. Exhaust fumes on drillfloor." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 66m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Recessed operations due to exhaust fumes on drillfloor." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up 3rd double - lower std joint #2 and splash zone jnt with simulatneous lift by deck crane and TDS." "On 2008-08-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 95m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH with production riser to 95 m. Hung off production riser in riser spider. Removed handling flange type E." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 95m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up 4th double - upper pup joint and tensioner joint with simultaneous lift by deck crane and TDS." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 95m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH with production riser to 118 m. Hung off production riser with hang off plate in riser spider." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed handling flange. Picked up stand with premade running flange. Made up flange to tensioner joint. Picked up weight and removed hang off plate." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH on 5 1/2' DP stand to land TBC on wellhead. Observed with ROV and used pusher tool to help TBC to enter riser guide funnel. Observed in riser guide funnel window while coming down. Ran TBC to +/- 10 cm above bottom of window." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Released 6 MT guidewire from template and ROV hook on riser guidewire clamp. Retrieved guidewire to surface. Released 10 MT guidewire." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Hooked 10 MT guidewire on funnel. Removed RLGF. Oriented TBC ROV panels by rotating 1/8' turn counterclokwise. Ran and established hotstab in TBC receptacle." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Landed TBC/production riser on wellhead and set down 15 MT. Verified TBC fullly landed by oserving marker/band on TBC. Locked TBC connector by pressurising port A1 to 2500-3000 psi. Observed upwards movement on TBC upper body when locking TBC." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Took 10 MT overpull on TBC to verify locked." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Moved hotstab to port B1 and flushed lower dog cavity and upper piston cavity according to Vetco procedure." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Measured and marked groves on tensioner joint. Installed centralizer and boat collision stool in Centralizer deck. Made up contact ring. Made up tensioner assembly half hubs. Raised tensioner assembly to contact ring using tensioner cylinders. Adjusted pressure to 90 bar and transferred tension from block to tension cylinders. Installed centralizer in Tensioner deck." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up TDS to landing strand. Filled production riser with seawater pumping from cement unit." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested production riser against VMB plug to 20/345 bar 5/10 min - ok." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Measured and marked tensioner joint 141,4 cm above Tensioner deck. Rigged up, adjusted and dressed Norse cutting equipment on tensioner joint. Barriered off area. Adjusted block weight to put slight overpull at cut height. Drained riser through port on running flange." "On 2008-08-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Cut riser according to Norse cutting procedure. Retrieved cut part of tensioner joint. Removed riser spider. Installed outer ring and masterbushing. Broke out landing stand. Laid out cut part of tensioner joint. Installed hole cover in RT." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Put debris barrier inside tensioner joint. Re-configured cutting jig for making bevel. Cut bevel. Used handtools to dress cut and bevel. Removed cutting jig, cleared and tided Tensioner deck." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled master bushing and outer ring. Transferred 2 x annulus valves to Tensioner deck using tugger." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed lift cap and single joint elevator on 13 3/8' multibowl. Attached 2 tuggers for dual lift in order to avoid F-4 shut in. Lowered 13 3/8' multibowl from drillfloor to well head. Slipped multibowl over tension joint and adjusted to correct orientation 45 deg aft stb." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Retrieved tuggers. Installed F-5 hatch on Weather deck." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Pressure tested BT seals in multibowl to 35 bar - ok. Injejected and energized plastic in upper and lower BT-seals. Tested BT seals to 3000 psi / 10 min - ok. Locked in 1000 psi between BT seals. Energized multibowl slips by torquing up cap srews to 600 ft-lbs." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed outer ring and master bushing. Removed hatch on Weather deck." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH with 5 1/2' stand and made up to multibowl running tool. Performed overpull test of 5 MT on multibowl - ok." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Broke multibowl running tool with chain tong. Pulled running tool on 5 1/2' stand. Broke out and laid out running tool. Racked back 5 1/2' stand." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Confirmed measurement from RT to 13 3/8' wellhead to 19,955 m using laser." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed hatch on Weatherdeck." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed slings for installing BOP riser. Prepared for dual lift in order to avoid shut in of F-4/F-14. Attached 75 MT shackle in each bail. Primary lift sling 30 MT shackles + 10 m / 10 MT sling attached to 7,5 MT pad eyes with 25 MT shackles. Secondary lift sling in each bail - 12 MT shackle + 11 MT sling + 8,5 MT sling + 11 MT sling choked around neck of BOP/NT-2 connector." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Installed VR plugs, blind flange and annulus valves on wellhead outlets and tested each component accordingly." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Inspected TDS for loose items after maintenance." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk for lifting and installing BOP joint." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed hatch on Weatherdeck. Removed outer ring and master bushing in RT." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Ran surface riser with TDS and dual lift to 0,5 m above 13 3/8' wellhead. Removed hole cover and cleaned seal surface. Installed seal ring. Alligned connector and landed NT-2 connector." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up NT-2 connector according to Vetco procedure. Took 2,5 MT overpull on connector." "On 2008-08-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Barriered off wellhead module. Installed split hatch on Weatherdeck. Built scaffolding on Weatherdeck for access to BOP connection." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Covered scaffolding with canvas. Covered gap between riser and Weatherdeck with aluminum cover. Released BOP stump connector." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Skidded BOP from STB setback area and landed on BOP riser." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Made up BOP connection. Meanwhile made up swadge to TDS and tested upper/lower IBOP and standpipe to 20/345 bar 5 /10 min." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Hooked up up BOP tension cylinders to BOP. Made up bell nipple spool. Installed and made up overshot joint to BOP. Prepared for installing diverter." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged up slings for installing diverter. Ran diverter." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk / shift hanover meeting." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Continued making up overshot joint and diverter." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up 13 3/8' BOP testplug. Cleaned drains inside/outside drillers cabin due to bad smell." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH with 13 3/8' BOP test plug on 5 1/2 DP stand and landed in surface wellhead at 20 m MD." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lined up cement unit to BOP kill inlet and filled prodcution riser and BOP with seawater prior to pressure test." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Closed MPR. Pressure tested BOP connection 35/345 bar 5/10 min - ok." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Strapped pipe according to Vetco instructions. Strapped RT to landing point to 20,46 m MD, but questioned value." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Function tested BOP pipe rams and annular." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Re-strapped pipe according to Vetco instructions. When puttig on hole cover the hinged lid came loose and was lost into the riser/well." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- other' and lasted for 3.8 hours. Operational details: Item lost in hole was a steel plate of 18 x 20 cm. Discussed situation and made plan for attempting to fish. Found that clearance (6 mm) between the riser and the 13 3/8' BOP test plug would make it impossible for the lid to pass the plug. Drained BOP to get dry access to BOP through ram door. Prepared fishing magnet on rope." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Opened LPR ram doors. Drained riser. Picked up to 11,5 m MD in order to get pictures of fish. Got pictures showing lid resting on top of 13 3/8' test plug." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Picked up in steps to +/- 10 m and took pictures through bonnet door for each incremental movment to observe position of fish. Observed lid leaning over into the larger 18 3/4' ID close to the BOP, i.e. in position to attmept fishing with magnet. Put magnet on rope into riser through ram door. Latched fish with magnet and caught through ram door." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Inspected fish and found that the pin in the broken hinge was still missing. Estimated missing pin to be 26 mm x 9 mm OD. Discussed situation. Decided to continue picking up in small increments in case pin was caught in the lip seal of the 13 3/8' test plug." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Picked up in steps of 1-2' and took pictures through bonnet door accordingly. Picked up to lips seal was visible in larger riser ID, but found no evidence of pin being trapped in lip seal." "On 2008-08-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: POOH with 13 3/8' test plug. Observed for lost pin through ram doors when passing LPR with 13 3/8' test plug. Pulled 13 3/8' test plug to surface. Found small brass washer originating from the broken hinge on top of the plug. No pin recovered (later found missing pin trapped behind lip seal). Closed doors on LPR." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Inspected 13 3/8' plug and found worn lip seal. Broke out and laid down plug. Traced and made up back up 13 3/8' test plug. Closed doors on LPR." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: RIH with 13 3/8' test plug and landed in surface wellhead at 20 m MD. Lined up cmented unit and filled BOP with seawater through kill line. Closed UPR. Pressure tested BOP against test plug to 20/345 bar 5/10 min. Observed leakage possibly from BSR ram door/bonnet. Bled off pressure." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pressured up to 345 bar in order to locate leakage. Located leakage possibly across BSR ram door." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Drained BOP. Opened BSR doors. Inspected and cleaned seals, found no evident damage. Closed BSR doors." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Lined up cement unit and filled BOP with seawater. Pressure tested BOP to 345 bar / 10 min -ok. Observed and found leak to be from the BOP hydraulic system." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH with 13 3/8' test plug and strapped pipe according to Vetco instructions." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Strapped pipe according to Vetco instructions. Calculated 10 3/4' landing point to be 20,866 m RT." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up bowl protector seetting tool and made up to 13 3/8 bowl protector." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 13 3/8' bowl protector at 20,44 m MD. POOH and laid down running tool." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleared and tidied drillfloor. Held toolbox talk prior to racking back tie-back tools." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up and made up 10 3/4' Itco spear to stand of 5 1/2' DP. Racked back in derrick. Cleaned windows on drillers cabin for safety due to poor visiblity." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up adjustment sub actuation tool to 5 1/2' DP stand. Racked back in derrick." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for picking up 10 3/4' casing hanger / adjustment sub." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up up 10 3/4' casing hange / adjustment sub and hung off in rotary.Made up casing hanger handling tool accroding to Vetcc instructions. Laid out assembly." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for running annulus insert retrieval tool." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Made up annulus insert J-slot retrieval tool and RIH 5 1/2' DP. Strapped pipe and checked serial numbers when running in." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Landed off at 139,89 m MD and engaged J-slot tool according to Vetco instructions. Pulled free annulus insert." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with annulus insert on 5 1/2' DP and strapped pipe to check measurements. Calculated tie-back adapter no-go to 139,75 m MD." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out and laid down annulus insert and retrieval tool." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up jet sub to stand of 5 1/2' DP." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with jet sub on 5 1/2' Dp from surface to subsea wellhead 140 m MD. Made 6 passes +/- 2m across subseawellhead while circualtion at 3000 lpm / SPP 22 bar. Displaced production riser to TSW by circualting 3000 lpm / 22 bar. Pumped a total of 50 m3 TSW." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with jetting sub from 140 m MD to surface. Broke and laid out jet-sub." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with bowl protector pulling tool. Engaged bowl protector. Strapped pipe in and out to 20,44 m (20,86 m to 10 3/4' casing hanger lading point)." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with bowl protector. Broke and laid out bowl protector and running tool." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Lifted 10 3/4' casing tong to IR rails. Rigged up BX elevator. Removed master bushing and installed FMS in rotary and hooked up same. Hooked up and function testred casing tong. Re-arranged and tested HTS rollers." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 10 3/4' tie-back adapter using tugger and single joint elevator. Removed protector and inspected thread and O-rings. Hung off in FMS and secured with dog collar." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to running tie-back casing." "On 2008-08-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Ran 10 3/4' - C95 60,7# VamTop tie-back casing to 15 m MD." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Ran 10 3/4' - C95 60,7# VamTop tie-back casing from 15 m to 99 m MD." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and made up 10 3/4' 8,89 m space out pup." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Removed BX elevator and changed to DP elevator. Picked up 10 3/4' casing hanger / adjustment sub assembly and made up same. Removed rubber protection and checked casing hanger according to Vetco proecdure." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up stand with 10 3/4' Itco spear with PRS. Made up TDS while holding stand with PRS." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH and engaged spear in 3 m pup joint below 10 3/4' hanger by rotating string counterclockwise while picking up, obtained weight of tie-back string of 80 MT. Noted block height when casing hanger flush with RT." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with tie-back casing on Itco spear and tagged tie-back threads at 139,8 m with 2-3 MT (i.e. approx 15 cm deeper than expected). Checked colour band through B-annulus on Tensioner deck, observed centre of 2nd orange band." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Put horizontal and vertical mark on pipe to count turns and measure elevation. Started rotation at 3 rpm clockwise and counted turns. Lost grip on Itco spear due to too much weight being slacked off when the block weight increased. Re-engaged spear by conterclockwise rotation. Resumed rotation and let block weight incrase approx 8 MT. Stopped rotation after an estimated 4-5 turns obtained, judging from effective rotation and travel on colour bands. Took overpull to 10 MT and set torque limit to 10,17 kNm. Resumed rotation at 3 rpm. Torque and weight increased and peaked at 7,03 kNm before Itco spear released. Estimated total downwards travel 2,5-3 inches. Re-attempted torquing up tie-back adapter twice, spear released at 3-5 kNm. Re-engaged spear and took overpull on tie.back adapter to 30 MT." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released 10 3/4' Itco spear and POOH with same. Racked back stand in derrick. Prepared for rigging down casing tong." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Rigged down casing tong. Removed FMS and installed master bushing and bowl. Picked up adjustment sub actuation tool. Made up TDS." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with adjustment sub actuation tool to 28,72 m MD to locate actuation dogs in polish bore (1st target)." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pressured up through DP to 140 bar to actuate horizontal latch dogs." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up to 2nd target and confirmed horizontal dogs latching into profile, took 5 MT overpull. Confirmed measurements. Rotated pipe 3 turns clockwise and obtained 2 kNm torque. Bled off pressure on DP to zero. Checked measurement towards rotary - no movement." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rotated pipe clockwise to retract adjustment sub. Obtained 6,5 turns on adjustment sub before stalling out on 10 kNm. Took 30 MT overpull and rotated 1/8 turn clockwise before stalling out at 6 kNm. Continuosly checked colour bands through annulus outlet on Tensioner deck. Checked elevation of casing hanger -ok." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Slacked off overpull and came down to 1st tool target (sealbore). Waited 2 minutes for horizontal dog crest to relax. Picked up again and got unexpected overpull of 4-5 MT 20 cm above 2nd tool target (latch groove). Slacked off pipe and picked up againg in attempt to free tool, got overpull at 2nd tool target. Made several attempts to free pipe by coming up and down with tool, not able to pass 2nd target. Pressured up on pipe to 120 bar. Re-attempted passing 2nd target - negative. Bled off pressure. Worked pipe with +/- 5 MT at 2nd target - not able to pass. Tool was free to move down." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Discussed situation with town. Made plan of action." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Re-attempted comming free with adjustable sub actuation tool. Attempted to pull with 10 MT overpull - negative. Pressured up pipe to 115 bar twice in attempt to manipulate horizontal latch dogs. Worked pipe several times with ~ 10 MT overpull - not able to pass 2nd tool target." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held planning meeting for discussing contingency operations. Made plan of action." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held toolbox meeting prior to contingency operations." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressured up on DP to 130 bar to make sure horizontal latch dogs and vertical torque dogs engaged in adjustable sub profiles, maintained pressure throughout operation. Adjusted block weight to 81 mT (~1 MT overpull). Extended adjsutable sub while rotating 1-2 rpm / torque 2-3 kNm. Observed torque peak of 7,09 kNm when rotation and torque transferred to tie-back adapter. Verified correct 10 3/4' casing hanger travel by observing colour bands through annulus outlet." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with 10 3/4' tie-back casing on 5 1/2' DP stand from 140 m to 119 m MD. Hung 10 3/4' casing in manual casing slips and secured with dog collar. Observed top of casing hanger packed with dirt/cuttings. Moved casing tong to access IR." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed C-plate on top of 10 3/4' casing hanger. Bled off pressure on DP to zero. Adjusted pipe height to access 1st DP single with IR. Broke connection on 1st single (service breaking). Hung off DP in C-plate and screwd out connection with chain tongs. Racked back 5 1/2' DP double." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Installed DP elevator between C-plate and DP coupling and secured with cargo straps. Installed 10 3/4' BX elevator underneath 10 3/4' casing hanger. Removed drilling bails and DP elevator. Installed 10 3/4' BX elevator. Installed long bails and connected to 10 3/4' BX elevator. Moved casing tong to IR rails. Hooked up casing tong." "On 2008-08-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: POOH with 10 3/4' tie-back casing to access coupling underneath 10 3/4' casing hanger /adjustable sub assembly. Hung off on manual slips and secured with dog collar." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke casing connection while rotating pipe/bails counterclockwise with TDS. Pulled out until adjustment sub actuation tool in heigh with casing coupling. Observed horizontal latch dog profile packed with cuttings/dirt. Took pictures for reference. Removed dirt/cuttings as required." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Discussed situation. Decided to pull 10 3/4' tie-back casing for cleaning well." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ripped off horizontal dog latch crest. Stabbed adjustable sub actuation tool into 10 3/4' casing. Made up casing coupling. Landed 10 3/4' casing hanger in slips and secured with dog collar." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Removed long bails and BX elevator. Rigged up short bails." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to laying out DP single (innerstring)." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Connected bails to DP elevator on top of C-plate. Removed cargo straps. Pulled out DP single with adjustable sub actuation tool and laid out same. Removed C-plate." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up casing hanger handling tool and made up to 10 3/4' casing hanger. POOH to 110 m MD. Broke connection between assembly and 10 3/4' space out pup." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to POOH with 10 3/4' tie-back casing. Changed to 10 3/4' BX elevator." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with 10 3/4' tie-back casing from 110 m to 87 m MD." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with 10 3/4' tie-back casing from 87 m MD to surface." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging down casing running equipment." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged down casing tong. Removed 10 3/4' BX elevator and installed DP elevator. Cleaned and tidied drillfloor." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up bowl protector RT and made up to stand of 5 1/2' DP. Made up bowl protector to RT." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with bowl protector on 5 1/2' DP stand and landed same at 20,44 m MD." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with bowl protector RT, broke and laid out same." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Made up Vetco jet sub. RIH with jet sub and located across BOP. Made 3 passes across BOP cavities while pumping at 4600 lpm / SPP 62 bar." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with jet sub on 5 1/2' from 10 m to 140 m MD. Made up TDS to each stand. Washed down with 3300-3900 lpm / SPP 26-38 bar." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Washed across subsea wellhead/tie-back threads at 4000 lpm / SPP ~32bar, made 5 passes. Pumped 4 m3 hi-vis pill. Displaced production riser to TSW." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with jet sub on 5 1/2' DP and laid out same. Cleaned and tidied drillfloor." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up bowl protector RT to 5 1/2 ' stand. Pulled bowl protector at 20,44 m, broke and laid out RT." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Made up jets sub. RIH with jestsub on 5 1/2' DP stand. Made 2 passes across surface wellhead pumping 3600 lpm / SPP 39 bar. POOH with jetsub." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for laying out jetsub." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Laid out jetsub. Cleard and tidied drillfloor." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up adjustment sub actuation tool on single. Broke single and laid out actuation tool. Made up single to double to get full stand. Made up back-up adjustment sub actuation tool dressed with new horizontal latch ring. Racked back tool and 5 1/2' DP stand." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging casing running equipment." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Changed to 10 3/4' BX elevator. Installed PS-30 slips dressed for 10 3/4' casing. Lifted casing tong onto IR rails and hooked up same." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to running 10 3/4' tie-back casing." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Lifted back-up tie-back adapter onto HTS." "On 2008-08-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 39m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Ran 10 3/4' - C95 60,7# VamTop tie-back casing from surface to 39 m MD." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Ran 10 3/4' - C95 60,7# VamTop tie-back casing from 39 m to 108 m MD." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up 10 3/4' casing hanger / adjustment sub assembly with handling tool. Made up assembly. RIH to 119 m MD and hung off in RT. Broke off casing hanger handling tool with chaintong and laid out same. Drained riser by opening annulus valves." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up stand with spear in TDS and made up to TDS. Engaged spear in pup joint below 10 3/4' casing hanger (i.e. 3 m in from top of hanger)." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 10 3/4' casing hanger on spear. Tagged tie-back threads with 3-4 MT at 139,7 m MD, i.e. approx 10 cm shallower than expected. Attempted to rotated clockwise with 2700 Nm, stalled out after 1/4 turn. Rotated counterclokwise 1/2 turn, worked string and came approx 10 cm further down (corresonding to previous landing datum). Resumed clockwise rotation at 3 rpm and entered threads within 2700 Nm limit. Slacked off weight accordingly for each 2-3 MT gained on block. Observed color bands through annulus outlet to confirm travel and height." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Increased torque limit to 10170 Nm. Pulled 5 MT overpull and resumed rotation. String stalled with 7 kNm+ (6,52 kNm Nm recorded on Geoservice screen). Increased to 2 MT overpull, resumed rotation - stalled out on approx 3 kNm and spear released. Re-enaged spear. Took 13 MT overpull and resumed rotation, stalled out on 8 kNm+ (5,72 kNm recorded on Geoservice screen). Took overpull to 30 MT." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released spear and POOH. Broke out TDS connection and set back stand and spear in derrick." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up stand with adjustable sub actuation tool in PRS and made up to TDS. Measured in to 1st tool target." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressured up pipe to 140 bar to activate the adjustment sub actuation tool. Picked up to 2nd tool target to engage horizontal latch dogs and torque dogs. Observed 3-4 MT overpull at 2nd tool target. While maintaining overpull started rotation with 1 rpm. Rotated 2 turns / ~1 kNm. No movement observed on hanger at Tensioner deck. Wrong indications. Reattempted setting sequence with same negative result." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made another attempt on adjustable sub setting sequence. While maintaining overpull rotated 7 turns and retracted adjustment sub as per procedure." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Bled off pressure in DP, slacked off 1 m and waited 3 min to allow lock ring to be fully retracted. PU and POOH with adjustment sub actuation tool. Cleaned and cleared rig floor." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RD csg tong. Changed from PS30 slips to to master bushings. Broke down and LO spear and adjustment sub." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PU and MU HRT. RIH with HRT on 5 1/2' HWDP from surface to 20,77 m. MU HRT to 10 3/4' surface hanger by 10 left hand turns." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: MU TDS. Performed tool box meeting before lining up to test 10 3/4' tie-back csg. Verified line-up and pressured up to leak test 10 3/4' surface tie-back csg and 10 3/4' x 9 5/8' csg against VMB plug to 380 bar/10 min with cmt unit. 900 ltrs pumped. Test failed." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed line test to 380 bar/10 min with cmt unit. Test failed." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Greased surface valves on STP manifold and performed line test. Test failed." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: RU pump-in sub and hose directly from cmt test line. Performed line test to 380 bar/10 min with cmt unit. Ok." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Performed line test to 380 bar/10 min with cmt unit. Ok. Leak tested 10 3/4' surface tie-back csg and 10 3/4' x 9 5/8' csg against VMB plug to 380 bar/10 min with cmt unit. Ok. 605 ltrs pumped and 560 ltrs bled back." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Released HRT by 10 right hand turns. POOH and LD same. RD cmt line." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RU to RIH with 10 3/4' MS-T seal assy RT. Found RT dressed for pulling MS-T seal and had to re-adjust length to fit the latch dogs." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Re-adjusted length on RT to fit the latch dogs to be able to run MS-T seal. Meanwhile held Time-out for safety (TOFS) on rig floor and discussed lifting and tugger handling." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued RU to RIH with 10 3/4' MS-T seal assy RT." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with seal assy RT and MS-T seal from surface to 20.77 m. Landed out on 10 3/4' csg hanger and locked RT into riser. Sat MS-T seal by applying 4300 psi. Tested seal through test port in multibowl to 380 bar/10 min. Ok." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Released MS-T seal RT from 10 3/4' csg hanger and POOH with RT. LO RT and removed hydraulic hoses." "On 2008-08-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box meeting. MU and RIH with secondary bowl protector from surface to 20.53 m. Installed secondary bowl protector in surface wellhead. POOH and racked back RT. Cleared rig floor of excess equipment." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box meeting prior to retrieving VBM plug. MU VBM plug RT to 5 1/2' HWDP. Changed out master bushings for PS21 slips." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 632m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with VBM plug RT on 5 1/2' HWDP and 5 1/2' DP from surface to 632 m. Up weight 98 MR/down weight 93 MT/ 2.6 kNm at 10 rpm." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 632m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Established parameters and circulated 2x btms up (20 m3) at 2000 lpm/10 bar to displace out hi-vis pill on top of plug according to program." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 634m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with VBM plug on 5 1/2' DP from 632 m to 634.5 m. Attempted to latch on to and release VBM plug by applying 15-25 MT and washing above top of plug 200-2000 lpm /0.7 -9 bar between attempts. PU 2 m without observing any overpull after each attempt. Turned string 3 turns to aligne J-slot in RT. No sucess. A total of 10 attemps was made." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 632m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Latched on to and release VBM plug by applying 20 MT and then PU to 10 MT up weight on plug to verify that RT was properly latched on plug. Reduced weight on plug to 2 MT and pressured up DP to 30 bar (66 ltrs pumped) . Rotated DP 3/4' turn RH to open ball valve. Pressure dropped from 30 bar to 4 bar. Rotated 15 turns RH to release plug. Pulled up to 632,5 m and waited 10 min to allow elements to fully retract. RIH to 636.5 m to ensure that plug was free." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: POOH with VBM plug and RT on 5 1/2' DP from 632 m to OOH. Pulled PS21 slips, cleaned rig floor rotary and installed master bushings. LO VBM plug. Meanwhile changed inserts in PS30 slips to fit 7' tubing, inspected PRS and load tested manrider." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: MU and RIH with secondary bowl protector pulling tool from surface to 20.5 m. Pulled secondary bowl protector from surface wellhead. POOH and LO RT." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Held tool box talk before RU csg equipment. RU Odfjell csg tong and prepared to run 7' tubing. Connected torque/turn computer. Prepared manual slips for running completion assemblies. Lifted in place BOT cable drum on port fwd setback area." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 46m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: MU and RIH with 7 1/2' seal stem with ratcheting mule shoe assembly. Function tested ratcheting mule shoe. MU and ran two 7' tubing joints according to tally. MU and RIH 7' x 9 5/8' Granite production packer and one 7' tubing joint." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 505m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: RIH with 7' tubing in stds from 46 m to 505 m. Running speed was 5-8 stds/hr." "On 2008-08-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 891m. The activity was categorized as 'completion -- completion string' and lasted for 5.5 hours. Operational details: RIH with 7' tubing from 505 m to 891 m. Running speed was 6-8 jnts/hr." "On 2008-08-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1330m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: RIH with 7' tubing from 891 m to 1330 m. Running speed was 6-8 jnts/hr. Changed boxes on 2 jnts and rejecting 2 jnts." "On 2008-08-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2304m. The activity was categorized as 'completion -- completion string' and lasted for 15.2 hours. Operational details: RIH with 7' tubing from 1330 m to 2304 m. Running speed was 7-8 jnts/hr. A total of 4.0 hrs was used changing boxes on 5 jnts and rejecting 5 joints. Inspected joints on deck and found 5 jnts with potential damaged box end.Serviced and greased csg tong and elevator." "On 2008-08-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2306m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Held tool box talk prior to lifting in DHSV assembly. PU and MU DHSV assembly. RIH with DHSV assy through rotary and installed one joint above DHSV. PU DHSV to working height. RU sheave wheel in tugger and stabilized using aft PRS. Flushed and connected control line." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2306m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Tested CL to 520 bar/10 min. Ok. Bled down pressure to zero. 240 ml bled back. Pressured up CL to 345 bar to keep DHSV open. Isolated PS30 slips guide insert and made final adjustments to position slips and sheave in derrick." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2648m. The activity was categorized as 'completion -- completion string' and lasted for 5.0 hours. Operational details: RIH with 7' tubing, TRSCSSV CL and clamps from 2306 m to 2657 m. Running speed was 6 jnts/hr. Kept 345 bar on CL to maintain DHSV open while RIH." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2758m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: RIH with 7' tubing, TRSCSSV CL and clamps from 2657 m to 2758 m. Running speed was 6 jnts/hr. Kept 345 bar on CL to maintain DHSV open while RIH. Performed final count of tubing jnts. Moved HTS and rollers." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2812m. The activity was categorized as 'completion -- completion string' and lasted for 3.2 hours. Operational details: Installed swedge and space-out stand and made up to TDS. Started to circulate 200 lpm using mud pump. RIH with space-out string and stung into top of liner at 2812 m. Sat down 5 MT. Measured distance from top of tubing to mark on space-out string to be 39.25 m." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2812m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: PU and MU selected jnt and pup-jnts according to calculated space-out." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Changed from PS30 to master bushings. PU tubing hanger with handling tool and MU to last jnt of tubing sitting in the slips. Secured control lines with a clamp on upper tubing coupling. Lowered TH down to working height." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Cut CL 3 m above TH and fed CL through TH swagelok fittings. All spare penetrations was plugged onshore. MU fittings and leak tested all penetrations/fittings through 1/8' test port 35/380 bar 5/10 min using BOT pump. Ok. Installed C-plate and landed off TH. BO handling tool and LO same. Wrapped CL 3 times around hanger neck." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed communication collar onto TH by rotating 5 turns clockwise. Connected DHSV CL to 1/4' communication port at btm of communication collar. MU THRT to communication collar using 8 turns counter clockwise." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2812m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Connected DHSV CL to 1/4' communication port on top of THRT. Connected hydraulic test pump and pressure tested DHSV CL to 570 bar/10 min. Ok. Bled back 420 ml. Connected THRT lock/unlock lines from Vetco reel to THRT. Left 570 bar in DHSV CL while RIH." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: PU C-plate and RIH with TH. Cleared rig floor of excess equipment. PU and MU landing jnts. Up weight 180 MT/down weight 135 MT. RIH with TH. Tagged top of liner with 5 MT. Made 3 shifts with ratcheting muleshoe before stung into liner PBR and landed TH on no-go shoulder in multibowl. Slacked off weight until fully landed out. Verified correct TH land off and TH seal integrity by leak testing through port #1 and #2 on multibowl to 70 bar/5 min. Bled off pressure in all CLs. Pressured up function line to 3000 psi to engage TH lock down ring. Performed pull test on TH to 15 MT to verify hanger lock down." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pressure tested TH seal through test port #2 in multibowl to 35/380 bar for 5/10 min. Ok. Meanwhile lined up from cmt unit to well and flushed lines." "On 2008-08-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Performed line test aginst lo-torque valve on pump-in sub to 380 bar/10 min. Dropped 1.7 bar/10 min. 85 ltrs pumped. Opened lo-torque valve. Pressured up to 50 bar/5 min to check for pressure integrity prior to setting packer. Ok. 550 ltrs pumped due to tubing drained when landing TH." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 2.2 hours. Operational details: Closed DHSV and bled off above to 5 bar above. 120 ltrs bled back indicating DHSV not closed. Opened DHSV and pressured up and equalized above to 50 bar. 120 ltrs pumped. Observed drop in pressure on BOT pump indicating DHSV open, but had only 280 ml bled back. Repeated sequenze 2 more times before we got good indication that DHSV was fully open and had 220 ltrs bled back. Repeated function test of DHSV. Closed DHSV and bled off above to 5 bar. 80 ltrs bled back. Observed for 10 min to confirm that DHSV was fully closed and not leaking. Ok. Opened DHSV and pressured up and equalized above to 50 bar. 80 ltrs pumped. Observed drop in pressure on BOT pump indicating DHSV open. Bled off pressure down to 5 bar. 220 ltrs bled back." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.2 hours. Operational details: Pressured up tubing from 5 bar to 380 bar. 1386 ltrs pumped. Kept 570 bar on DHSV CL. Held pressure for 15 min to set packer and test tubing. Ok. Had 1.3 bar drop. Observed load vibration noise on rig floor when pressure reached 260 bar. Investigated TH and all well head levels. No findings. Bled off tubing pressure and observed pressure dropped immediately to zero. Concluded that lead target blocked cmt line. This was in accordance with observed noise. Bled off tubing pressure carefully to zero. Had 1360 ltrs bled back." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Lined up through cmt kill line. Performed line test 30/380 bar for 5/10 min. Had 1.4 bar drop." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Pressured up tubing to 330 bar while keeping 570 bar on DHSV CL. 1157 ltrs pumped. Closed DHSV and bled off pressure above DHSV to 260 bar. 20 ltrs bled off. Inflow tested DHSV to 70 bar diff/15 min. Had 1.3 bar drop. Bled off pressure above DHSV to 10 bar. 140 ltrs bled back. Inflow tested DHSV to 320 bar diff / 30 min. Had 0.1 bar increase. Equalized pressure by pressuring up to 330 bar above DHSV and opened DHSV. 220 ltrs pumped. Bled off pressure in tubing to zero and kept DHSV open with 570 bar. 1000 ltrs bled back." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Lined up cmt unit to A-annulus, with hose connected to multibowl and tested RU to 35/380 bar for 5/10 min against annulus valve. Vented B-annulus." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Performed line test to A-annulus to 35/380 bar for 5/10 min against annulus valve using packer fluid. High pressure test dropped 1 bar in 10 min. Opened B-annulus to vent." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- test scsssv' and lasted for 2.8 hours. Operational details: Pressured up A-annulus to leak test packer from below and TH from below to 35/380 bar for 5/10 min pumping brine at 70 lpm. Kept tubing open on drill floor and 570 bar on TRSCSSV CL. Pumped 117 ltrs and observed 0.01 bar drop on low pressure test. Pumped 1170 ltrs (total) and observed 0.5 bar drop on high pressure test. Had flow on both tubing and B-annulus while pressuring up A-annulus due to ballooning effect. No flow observed when pumps was shut in. Bled pressure down to zero and had 1100 ltrs in return. Bled off and shut in A and B-annulus. Closed TRSCSSV. Had leak in FWD PRS." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Worked at hight and repaired hydraulic leak in FWD PRS." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box meeting. Released landing string by 9 right hand turns. POOH and LD landing string." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: RD Odfjell csg tong and control box. RD tubing handling equipment." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box meeting. Changed to 5 1/2' handling equipment. PU and MU XO 5 1/2' FH box x 3 1/2' IF box to centralizer / BPV running adaptor / BPV. RIH and landed BPV on 5 1/2' DP in TH at 20.3 m. Sat down string weight to extend locking keys and energized seals. Rotated string 8 1/2' turns clockwise to lock mandrel and free running adaptor in J-slot. POOH with running string and LD RT." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: PU 2 joints of 5 1/2' HWDP and RIH and drained riser. LO jnts. Meanwhile cleared rig floor of CL wheel, protectors and x-overs. Prepared slings for diverter and double lift for surface riser." "On 2008-08-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Held tool box talk. Attached slings to slick joint. Prepared barriers, handrails and slings. Pulled diverter and secured in set back area. Installed outer ring and master bushings. Loosened nuts on slick joint. Disconnected tension cylinders in WH module. Pulled slick joint and secured in set back area. ND NT2 connection on BOP and sat on stump." "On 2008-08-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued setting BOP on stump." "On 2008-08-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Connected slings to riser joint and removed scaffolding on NT2 connection in moonpool." "On 2008-08-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Disconnected NT2 connector on riser joint and pulled riser jnt to rig floor using double lift. Installed master bushings on rig floor and hatch on weather deck. LD riser joint." "On 2008-08-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.8 hours. Operational details: Disconnected control lines from communication collar and hoisted same to rig floor through hole in half-moon hatch in moonpool. Installed anti vibration ring on TH. Removed one control line exit block on multi bowl. Unwrapped required length of CL around TH neck and fed control line through dedicated port on multi bowl. Fed high pressure packings and fittings onto CL and MU fittings to threads in multi bowl. Installed dart in BPV in TH by hand. Installed 137 VG seal ring on top of multi bowl and VG 63 seal ring on top of TH." "On 2008-08-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Removed master bushings on rig floor and one half-moon of hatch in moonpool. Lowered spacer spool down from rig floor with TDS and 6 MT tugger (dual lift) until NT2 box connector landed out on top of WH. MU locking dogs until connection leveled out. MU actuation screws with 800 ft-lbs." "On 2008-08-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Continued MU actuation screws with 800 ft-lbs. Disconnected slings and removed same. Pressure tested and energized BT seals through ports 7/8. Tested VG 63 connection trough test port 9/10 to 35 bar/5 min. Tested TH void, grafoil seals and BT seals 35/380 bar for 5/10 min via test port 5/6. MU ferrule swagelock fittings for CL. Installed seal rings and CL exit block. Installed seal ring on top of spacer spool. Meanwhile cleaned cantiliver before laying out 7 5/8' tubing. *** Operations transferred to F-99 ***" "On 2008-08-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed F-5 hatch on weather deck to allow XMT to pass through. Held tool box meeting. Lifted XMT over moon pool with port overhead crane. Transferred weight (XMT) from overhead crane to top drive (TDS). Lowered XMT down through weather deck hatch. Oriented and landed XMT on top of spacer spool. MU grayloc connection and disconnected slings from XMT. Pressure tested seal ring to 35 bar/10 min through test port #3 and #4 on spacer spool to confirm proper seal. Meanwhile prepared WL equipment and cleaned inside cantiliver and in pump room." "On 2008-08-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed flow line spool onto XMT using 6 MT tugger from rig floor. Re-installed hatches on F-5. Notified PCR for injection start up of F-4. Meanwhile MU and RB 1 stds of 7 5/8' csg (A total of 9 stds made up), prepared WL equipment and cleaned inside cantiliver and in pump room." "On 2008-08-21, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Connected flexible flow line to flow line spool. Meanwhile MU and RB 4 stds of 7 5/8' csg (A total of 12 stds made up), prepared WL equipment and cleaned inside cantiliver and in pump room." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Connected flexible flow line to flow line spool. Meanwhile MU and RB 7 stds of 7 5/8' csg (A total of 19 stds made up), lifted WL BOP's into moonpool and cleaned inside cantiliver and in pump room." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Opened HMV with Seawell test pump. Held tool box talk. Lined up from cmt unit and connected hose on KWV. Performed line test to 30/380 bar for 5/10 min against KWV. 3.0 bar drop (0.8%) on high pressure test ." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pressure tested XMT body and VG 63 ring to 30/380 bar for 5/10 min against dart in BPV. 2.0 bar (0.5%) drop on high pressure test. 50 ltrs pumped and approx 40 ltrs bled back." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Attempted to flush flowline through XMT by pumping pot water from production, but had installed check valve in front of hose from cmt unit to KWV. Removed CV and lined up from cmt unit to KWV. Performed line test to 30/380 bar for 5/10 min against KWV. 3.0 bar drop (0.8%) on high pressure test." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Open PWV. Flushed through flowline, PWV, XMT, KWV to cmt unit from production with pot water." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested flowline/XMT to 30/345 bar for 5/10 min. 3.6 bar (1.0%) drop on high pressure test. 95 ltrs pumped and 90 ltrs bled back." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Pressured up to 130 bar against BPV & dart. Close MMV and bled off pressure above MMV to 10 bar. Inflow tested MMV to 120 bar differential pressure for 15 min. Test ok. Equalized pressure above MMV. Opened MMV and closed HMV. Bled of any pressure above HMV to 10 bar. Inflow test HMV to 120 bar differential pressure for 15 min. Test ok. Equalized pressure across HMV. Opened HMV. Bled off pressure. Closed valves. Pressure tested BOT control line exit block for DHSV to 570 bar/15 min using BOT pump. Test ok. Closed DHSV. Bled off 335 ml on line." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Built scaffolding around XMT. Opened HMV. RIH with retrieving tool for dart on stinger and retrieved dart. POOH with dart. Pulled BPV from TH. Closed HMV and SV. Closed PWV, KWV and MMV." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Commisioned F-5 XMT. Meanwhile installed WL BOP's (tripple BOP below dual BOP). Built scaffolding around WL BOP's and installed riser sections to rig floor." "On 2008-08-22, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Commisioned F-5 XMT. Meanwhile LD 3 1/2' DP, installed BOP rams and cleaned lower shakers and moon pool area. Torture-tested 7/16' cable and cut off 1000 m." "On 2008-08-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Commisioned F-5 XMT. Meanwhile LD 3 1/2' DP (16 of 31 stds layed down), installed BOP rams and cleaned lower shakers and moon pool area. Built rope socket/cable head on 7/16' cable." "On 2008-08-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 11.0 hours. Operational details: Commisioned F-5 XMT. Meanwhile LD 3 1/2' DP (31 stds layed down) and cleaned lower shakers and moon pool area. Held TOFS due to dropped 3 1/2' DP in fox hole. Tested perforation toolstring and prepared WL equipment. Bundled up and removed 3 1/2' DP from cantiliver for backload." "On 2008-08-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Commisioned F-5 XMT. Meanwhile spotted equipment on rig floor and RU WL lubricator, grease skid, nitrogen rack and local control panel. Hot-checked perforation toolstring. Prepared for pressure testing WL rig up." "On 2008-08-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held tool box talk prior to pressure testing WL rig up and prior to making up guns." "On 2008-08-23, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Hooked up local control of DHSV and HMV on XMT. Removed hydraulic tube from HMV and drained hydraulic fluid. Hooked up DHSV control hose on XMT. Hooked up HMV control hose. Meanwhile lined up to fill riser and lubricator with cmt unit. Lifted toolstring into toolcatcher and MU lubricator to lower riser." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Tested DHSV local control hose to 520 bar - ok. Tested HMV local control hose to 207 bar - ok." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Opened SV and and verified line up by opening KWV with 10 bar on the line. Filled riser and lubricator with packer fluid using cmt pump. Closed KWV. Leak tested line from cement pump to KWV to 30/200 bar for 5/10 min against cloed KWV using packer fluid. 1.9 bar (0.95%) drop on high pressure test. 20 ltrs pumped." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Attempted to leak test WL rig up to 30 bar/5 min, but had visual leak between two lubricator sections. Changed O-ring in leaking connection without laying down lubricator. Leak tested WL rig up to 30/200 bar for 5/10 min using packer fluid and cmt pump. 1.8 bar (0.9%) drop on high pressure test. 30 ltrs pumped and bled back. Bled off pressure to closed drain. Closed SV and KWV." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Opened MMV using 42 turns. Opened HMV by applying 207 bar on CL using local control panel. Equalized above DHSV in steps up to 15 bar (60 ltrs pumped) and opened DHSV by applying 520 bar on CL using local control panel. Closed HMV and broke off lubricator at in-situ sub." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Perforation run #1: Lowered orientating weight and 30 ft gun section into lower riser section and hung off in C-plate. Connected and armed perforating guns according to Schlumberger procedure." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Perforation run #1: Connected lubricator and re-routed tugger on lubricator due to twist with wireline sheave wheel." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Leak tested in-situ sub to 30/200 bar for 5/10 min with Seawell test pump. Ok. Observed leak in XMT instrumentation piping. Installed temporary fitting." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3731m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Opened HMV and observed 0 bar WHP. Verified TRSCSSV was open. Opened SV and RIH with 4.5' TCP guns on 7/16' electric line from surface to 3731 m MD. Up weight 1225 kg / Running weight 1170 kg at 450 m." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3731m. The activity was categorized as 'workover -- perforate' and lasted for 2.8 hours. Operational details: Bled 52 bar WHP down to zero through closed drain. Correlated guns to shooting depth using GR. Hanging weight 2350 kg. Fired guns and perforated interval #1 from 3704.0 m to 3712.0 m MD. Positiv confirmation that guns had fired, but observed no increase in WHP." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.2 hours. Operational details: POOH and logged GR/CCL from 3700 m to 2809.5 m to top of liner (TOL). POOH with 4.5' TCP perforation guns from 2809.5 m to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum. Broke lubricator at in-situ sub. BO and LD guns using sertified lifting sub. Observed that all shots had fired." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Perforation run #2: Megged and inspected cable. Built and tested new cable head. Checked CCL on rig floor. Shut down power to Schlumberger unit according to procedure before MU perforation gun." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: PU gun sections from cantiliver onto HTS. Lifted guns into riser using fwd PRS. MU firing head and CAL-B to gun hung off in riser and armed gun. PU toolstring and lifted into toolcatcher. Connected and hung off orientation weight and second gun sections in C-plate. Connected upper toolstring to guns hanging in toolcatcher. PU tension on toolstring and took off C-plate." "On 2008-08-24, at Well NO 15/9-F-5, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Connected lubricator and filled with MEG. Tested in-situ sub to 30/200 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0.1 WHP. Verified TRSCSSV was open. Opened SV. RIH with 4.5' guns to 70 m below seabed and powered up logging unit." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3730m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: RIH with 4.5' TCP guns on 7/16' electric line from 250 to 3731 m MD. Up weight 25000 kg / Running weight 1550 kg." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3730m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Bled 52 bar WHP down to 2 bar through closed drain. Correlated guns to shooting depth using CCL. Hanging weight 2500 kg. Fired guns and perforated interval #2 from 3682.0 m to 3700.5 m MD. Positiv confirmation that guns had fired, tension dropped 50 kg and WHP dropped to 0.5 bar." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: POOH with 4.5' TCP perforation guns from 3680 m to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH. Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Broke lubricator at in-situ sub. BO and LD guns using sertified lifting sub. Observed that all shots had fired." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Perforation run #3: Megged and inspected cable. Built and tested new cable head. Checked CCL on rig floor. Shut down power to Schlumberger unit according to procedure before MU perforation" "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: PU gun sections from cantiliver onto HTS. Lifted guns into riser using fwd PRS. MU firing head and CAL-B to gun hung off in riser and armed gun. PU toolstring and lifted into toolcatcher. Connected and hung off orientation weight and second gun sections in C-plate. Connected upper toolstring to guns hanging in toolcatcher. PU tension on toolstring and took off C-plate." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Connected lubricator and filled with MEG. Tested in-situ sub to 30/200 bar for 5/10 min with Seawell test pump. Ok. Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened SV. RIH with 4.5' guns to 70 m below seabed and powered up logging unit." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3730m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: RIH with 4.5' TCP guns on 7/16' electric line from 250 to 3730 m MD. Up weight 2500 kg / Running weight 1550 kg." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3730m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Confirmed no WHP. Correlated guns to shooting depth using CCL. Hanging weight 2500 kg. Fired guns and perforated interval #3 from 3651.5 m to 3670.0 m MD. Positiv confirmation that guns had fired, tension dropped 50 kg." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: POOH with 4.5' TCP perforation guns from 3650 m to OOH. Powered down logging unit at 70 m below seabed. Made PA announcement and pulled cable head into tool catcher. Closed SV to verify BHA OOH. Closed HMV. Observed no WHP. Opened bleed to closed drain as a precaution. Opened needle valve and confirmed that lubricator was empty and that the well was on vacuum." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Opened HMV and observed 0 WHP. Verified TRSCSSV was open. Opened KWV. Pumped /bullheaded 3 m3 100% MEG at 100 lpm and 4-5 bar into well with cmt pump to provide cusion above closed TRSCSSV. Displaced MEG to above TRSCSSV by chasing it with 6.6 m3 packer fluid at 160 lpm and 5-6 bar. Pumped 1.2 m3 100% MEG to fill XMT body." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Closed TRSCSSV and HMV. Leak tested XMT cross to 130 bar / 10 min against closed HMV. Dropped 2.0 bar / 10 min (1.5 %). Bled off pressure to zero bar. Closed KWV." "On 2008-08-25, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Broke lubricator at in-situ sub. BO and LD guns using certified lifting sub. Observed that all shots had been fired" "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Continued to LD and observe 4.5' perforation guns. Changed out firing head with btm nose. Re-stabbed lubricator at in-situ sub." "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Lined up and leak tested line from cement unit to outer A-annulus valve to 30/380 bar for 5/10 min using packer fluid. 3.6 bar (0.95%) drop on high pressure test. 20 ltrs pumped. Opened inner and outer A-annulus. Ensured B-annulus was open. Monitored pressure on tubing side on lubricator. Pressured up A-annulus to 380 bar. Closed inner A-annulus valve. Bled off pressure to 5 bar to cmt unit. Inflow tested inner A-annulus valve to 380 bar for 30 min using packer fluid. 0.5 bar increase on test. 1190 ltrs pumped and 1100 ltrs bled back. No leak observed on B-annulus. Vacuum on tubing side. Equalized and opened A-annulus valve. Bled off pressure." "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: RD lubricatoor on rig floor. Disconnected and pulled riser sections above BOP to rig floor. Meanwhile brushed F-9 subsea wellhead before installing VX-ring." "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: RD hydraulic BOP hoses. Disconnected WL BOP's and transfered to overhead crane in moonpool. Meanwhile brushed F-9 subsea wellhead before installing VX-ring." "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Continued disconnecting WL BOP's and transfering them by overhead crane in moonpool." "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Removed manifold from XMT. Installed blind cap outside KWV and XMT tree cap with 1/2' needle valve on top. RU test hose from needle valve to Seawell test pump. Leak tested XMT cross to 35/380 bar for 5/10 min against KWV cap and XMT cap. Bled off pressure to zero. Closed needle valves and disconnected test pump. Closed KWV and SV. Meanwhile removed hatch and lifted out UWG reel, WL BOP's and half moon hatches from moonpool to main deck." "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Installed hatch on F-5 and continued removing WL equipment from moonpool. Meanwhile disassembled scaffolding bridges from cantiliver." "On 2008-08-26, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Transfered operation of HMV and TRSCSSV to platform system/production. Filled in and signed 'Well handover document' and handed over well from Volve D&W to Mærsk Production at 12:00. Meanwhile removed scaffolding around moonpool hatch. ****************END OF OPERATIONS****************" "On 2008-10-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.0 hours. Operational details: Top section of fwd PRS moved forward (along top-most track) until drive section released/broke off and fell over to the side, resting against the upper part of the derrick at midnight the 1. October on F-15S. F-5 frac job will be performed partly in parallell with Mærsk sorting out the situation with the fwd PRS." "On 2008-10-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.7 hours. Operational details: Prepared ropes and equipment in derrick to be able to put fwd PRS back in position. Meanwhile waited for supply boat to arrive with frac equipment. Continued to clear drill floor and perform general maintenance." "On 2008-10-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: Waiting for Westcon climbers to install ropes and equipment in derrick to be able to put fwd PRS back in position. Meanwhile cleared drill floor and performed general maintenance. Waited for supply boat to arrive with frac equipment." "On 2008-10-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Waiting for Westcon climbers to install ropes and equipment in derrick to be able to put fwd PRS back in position. Meanwhile serviced TDS, cleared drill floor and performed general maintenance. Waited for supply boat to arrive with frac equipment." "On 2008-10-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.5 hours. Operational details: Waiting for Westcon equipment to be unloaded from supply boat to be able to work on fwd PRS. Meanwhile removed pipe handler and link tilt cylinder on TDS and performed general maintenance. Waited for supply boat to unload frac equipment." "On 2008-10-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Waiting on helicopter operation before entering derrick with Westcon climbers." "On 2008-10-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Spotted Halliburton frac equipment in moonpool." "On 2008-10-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 8.8 hours. Operational details: Held tool box talk prior to RU for frac job on F-5. Checked frac equipment and made walkthrough with crew on spotting/rig up. Reviewed plans for rig-up. Meanwhile Westcon climbers installed ropes and equipment in derrick to be able to put fwd PRS back in position." "On 2008-10-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: RU 3' chicksan line in moonpool. Meanwhile Westcon climbers installed ropes and equipment in derrick to be able to put fwd PRS back in position." "On 2008-10-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: RU 3' chicksan line in moonpool. Meanwhile Westcon climbers installed ropes and equipment in derrick to be able to put fwd PRS back in position." "On 2008-10-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.0 hours. Operational details: RU hose from production to gizzly pumpes on cantiliver. Started to RU 3' chicksan line from grizzly pumps down through hatch to moonpool. Meanwhile cleaned and preserved tension system pad eyes, continued to work on TDS and prepared for barite injection." "On 2008-10-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 8.0 hours. Operational details: Continued to RU 3' chicksan line from grizzly pumps down through hatch to moonpool. Hooked up pump units electrically. Meanwhile cleaned and preserved tension system pad eyes, continued to work on TDS and prepared for barite injection in spud cans." "On 2008-10-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box talk prior to testing 9 5/8' csg on F-15S. Performed line test to 290 bar/5 min. Pressure tested 9 5/8' csg 290 bar/15 min. Dropped 2.2 bar (0.8%). 1760 ltrs pumped and 1760 ltrs bled back. Meanwhile connected Halliburton 4' suction hose to water production (Utsira water)." "On 2008-10-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Finalized hooking up pump units. Prepared T with pop-off for kill line. Meanwhile cleaned and preserved tension system pad eyes, continued to work on TDS and prepared for barite injection in spud cans." "On 2008-10-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 6.5 hours. Operational details: Crane could not operate due to high winds and thus could not continue RU in moonpool area. Prepared riser sections and pup-in subs on main deck. RU 3' chicksan line from grizzly pumps down through hatch to moonpool and test-started grizzly pumps. Meanwhile cleaned and preserved tension system pad eyes and started mixing barite batch #1 for barite injection in spud cans." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Crane could not operate due to high winds and thus could not continue RU in moonpool area. Prepared riser sections and 9 1/2' pup-in subs on main deck. Finished RU 3' chicksan line from grizzly pumps down through hatch to moonpool and test-started grizzly pumps. Ok. Meanwhile cleaned and preserved tension system pad eyes and mixed barite batch #2 for barite injection in spud cans." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: PU 9 1/2' riser sections from main deck and lowered into moonpool. PU 3' chicksan line from main deck and lowered into moonpool. Meanwhile cleaned and preserved tension system pad eyes and mixed barite batch #2 for barite injection in spud cans." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Production closed in F-5 and handed over well to drilling at 03:00." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Verified status on F-5 XMT with production operator. Opened bleed offs. Held tool box talk before rigging up on XMT." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Installed safety valve/pop-off on XMT kill side. Removed hatch cover from weather deck. Started installing 9 1/2' riser sections on XMT. Meanwhile cleaned and preserved tension system pad eyes and mixed barite batch #2 for barite injection in spud cans." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Removed tree cap and installed WL riser. Meanwhile abseilers evaluated derrick work, not able to continue working in derrick due to too high wind." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Built scaffolding to get access to WL riser connection." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Installed WL riser with two pump-in subs on top." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Built scaffolding to get access to the two pump-in subs." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.5 hours. Operational details: Rigged up 3' chiksan to the two pump-in subs. Filled Grizzly pump with diesel, using 1m³ ICB tanks. Secured all surface lines with wire. Meanwhile mixed last barite batch for STB spud can." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Performed SJA meeting with all involved personnel prior to leak test surface lines, and rate test Grizzly pumps combined with the Cmt unit. Meanwhile pumped barite into STB spud can." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Checked rig up / walked lines" "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Prepared for flushing the lines." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Held tool box talk with night shift prior to commence leak testing of the surface lines, and pump rate measurements of Grizzly pumps and Cmt Unit." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Flushed the lines to the Grizzly pumps." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Leak tested Grizzly pumps surface lines 35 bars 5min, increased pressure to 360 bars, observed minor leak at T piece in Moon Pool. Bled down pressure and tightened T piece." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Leak tested line to 360 bars 10 min. Closed Lo-torq at pop-off, attempted to leak test line to 380 bars. Found minor leak in line at cantilever. Bled off pressure and tightened Weco connection. Leak tested line to 380 bars 10min." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Lined up and leak tested line from Cmt unit to X-max tree. 35/360bars 5/10mins. Bled off pressure." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Opened the Swab valve, HMV and applied pressure to the DHSV control line." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Commenced pumping with the two Grizzly pumps at 500 lpm each pump. DHSV opened at 100 bars. Increased pump rate to 1000 lpm each pump. WH pressure 110 bars. Started pumping with the Cmt unit, pressure picked up to 135bars within a few minutes. Shut down the Cmt unit, observed that pressure dropped to 110 bars with 2000 lpm from the Grizzly pumps." "On 2008-10-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Investigated the pressure drop and found air trapped in suction line. Flushed suctions from Utsira manifold. Started pumping again. Lost suction when picking up the rate from 750 to 1000 lpm each pump. Opened fluid ends on Grizzly pumps and flushed manifolds. Made new attempt to pick up rate to 1000 lpm each pump, with same negative result as above." "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.8 hours. Operational details: Had several attempts to get rate reading from Grizzly pumps. Concluded that due to gas in the water coming from the Utsira manifold it was not possible to get proper suction. Flushed lines through PSV valve (#13). Meanwhile held toolbox talk with abseilers before starting working in derrick." "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Closed in the X-mas tree at the Swab valve. Production started water injection. Meanwhile rigged up to re-align forward PRS." "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 6.8 hours. Operational details: Production injected in F-5 well. To achieve stable injection rate and pressure prior to start frac operation. Parallel activity: Abseilers in derrick rigging up FWD PRS in preparation of re-alignment in upper section of derrick." "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.2 hours. Operational details: Held tool box talk and flow tested mix pump into Trip tank, flushed lines with sea water. Flow rate achieved 4000 l/min. Parallel activity: Abseilers in derrick rigging up FWD PRS in preparation of re-alignment in upper section of derrick. Cleaned in Moonpool, Shaker area, fluid end inspection on mud pumps, general maintenance." "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Held tool box talk and rigged down the suction line from Utsira manifold to Halliburton Grizzly pumps Parallel activity: Westcon down from derrick due to wind speed @ 34 knots," "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Held tool box talk and re-route suction line from Halliburton Grizzly pumps to the rig floor. Flushed CMT lines to drill floor, in preparation for frac job. Parallel activity: Westcon down from derrick due to too high wind speed." "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Continued flushing CMT lines to drill floor, in prep for Frac job. Parallel activity: Started to dilute 1.20 SG brine to 1.09 SG. Fluid end inspection on mud pump #1, Cleaned and preserved lifting eyes at wellhead." "On 2008-10-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Topped up Grizzly pumps with diesel. Built scaffolding tent for Halliburton controls on cantilever. Held tool box talk prior to derrick inspection of PRS, derrick beams, cable trays. Preliminary plan covered to move PRS into vertical position. Parallel activity: Prepared tools for removing hatch on Slurry tank." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Preparing pits with Brine and drill water for Frac job. Fixed Samson pump in pump room." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Derrick inspection to assess lifting point for cable trays, upper drive tray, bath tub. Listed extra lifting equipment needed in the derrick to come from Westcon." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Continued preparing pits with Brine and drill water for Frac job." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Westcon down from derrick due to too high windspeed. Continued further planning to move PRS into vertical position." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 8.0 hours. Operational details: Prepared plan/procedure for frac job on F-5. Mixed & diluted brine in pits to 1.09 SG. Parallel activity: Continued with Production injecting in F-5. Due to wind speed @ 37 knots no access to the derrick." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held tool box talk prior to perform frac job." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Lined up Halliburton lines & pressure test same to 330 bar 5 mins. Commence to perform frac job as per program." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Aborted frac job due to air in the suction system. Installed air bleed off line on both Halliburton Grizzly pump. Lined up for production to continue to inject F-5." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Continued injecting in F-5 via production. No access to derrick due to high wind speed @ 31 Knots. Parallel activity: Fluid end inspection on mud pumps, general maintenance, prepare pad eyes on tension deck and house keeping." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Held tool box talk prior to perform frac job." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Lined up for frac job, equalized across KWV and Swab, opened same. Commenced pumping 1.09 sg brine with Grizzly pumps at WI pressure 330 bars and took over from production. Production backed down injection and closed PWV, bled of pressure in flow line and opened bled valve on the flow line. Started to pump 700 lpm with Cmt unit 800 lpm with each Grizzly pump. WHP 330 bars." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Increased rate, Cmt unit 1000 lpm and Grizzlies 2070 lpm. WHP started to pick up slowly to 335 bars. Picked up rate at Grizzlies to 2300 lpm, pressure at suction line 0.9 bars. Started second mixing pump to keep up the suction pressure. Final pump rate: Cmt unit 1400 lpm Grizzlies 2400 lpm. WHP 349 bars, total pumped 380 m³ 1.09 SG brine." "On 2008-10-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Re-arranged surface suction line with two 4' lines coming from the rig floor. Commenced cleaning suction/mixing lines # 1 and mixing pump #3." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Prepared Suction line #2 and mixing pump #1 for transforming brine to the two 4' supply hoses to the Grizzlies. Unable to work in derrick due to high winds." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Abseilers worked in the derrick securing lifting equipment to move PRS to vertical position." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Removed hatch on Slurry tank, cleaned out skimmer tank. Cleaned lines for frac job in Pit room. Commenced taking on Barite from boat. Unable to work in derrick due to high winds." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 8.2 hours. Operational details: Recieved 102 MT Barite, 200m³ 1.20 SG Brine and 600m³ drill water. Continued with production, to inject on F-5 well. Parallel activity: Abseilers continued rigging up in preparation for alignment of FWD PRS, upper section of derrick. Fluid end inspection on mud pumps, general maintenance, prepared pad eyes on tensioner deck." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Halliburton preparing equipment on cantilever prior to frac job on F-5. Parallel activity: Abseilers down from derrick due to frac job F-5." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held tool box talk prior to start frac job on F-5." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Lined up for frac job, equalized across KWV and Swab, opened same. Commenced pumping 1.10 sg brine with Grizzly pumps at WI pressure 330 bars and took over from production. Production backed down injection and closed PWV, bled of pressure in flow line and opened bled valve on the flow line. Started to pump 500 lpm with Cmt unit and each Grizzly pump running at 750 lpm. WHP 331 bars." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Increased rate on Cmt unit in steps to 1400 lpm and Grizzlies 2400 lpm. Final WHP 357 bars, total pumped 409 m³ 1.10 SG brine. Parallel activity: Mount hoses on HP cleaning hose reel in shaker area." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Shut in well at XMT. Frac job performance according to plan, frac of the formation not achieved. Commenced to rig down Halliburton surface equipment." "On 2008-10-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.0 hours. Operational details: Continued rigging down Halliburton surface equipment. Parallel activity: No access in derrick due to high winds. Worked on mud pump #2, cleaned and preserved lifting eyes at wellhead. Continued cleaning out skimmer tank. Cleaned Rig floor equipment in sack store." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Continued rigging down Halliburton surface equipment in the Moon pool." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.8 hours. Operational details: Continued to rig down Halliburton equipment in Moon pool and on wellhead. Rigged down Seadrill riser, removed scaffolding. Parallel activity: Abseilers got access to the derrick for rigging up equipment for alignment of FWD PRS." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Continued to rig down Halliburton equipment in Moonpool and on wellhead. Snap Lock dropped from derrick. Took time out for safety with involved personnel." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Continued to rig down Halliburton equipment in Moonpool and wellheads Parrallel activity: Abseilers resumed work in derrick." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 7.0 hours. Operational details: Rigged down Halliburton surface equipment in the Moon pool. Parallel activity: Abseilers continued rigging up in preparation for alignment of FWD PRS, upper section of derrick." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Rigged down Halliburton surface equipment on the cantilever." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.8 hours. Operational details: Abseilers continued rigging up in preparation for alignment of FWD PRS, upper section of derrick." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Cleaned and preserved lifting eyes at wellhead, Removed drag chain support and brackets of overhead crane in Moon pool. Continued cleaning out skimmer tank. Abseilers unable to work in derrick due to high winds." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held pre-job meeting with new arrived WL personnel." "On 2008-10-12, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Prepared for rigging up WL equipment below the cantilever." "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.0 hours. Operational details: Prepared, Grease injection head for 7/32' wire, Rig up BCU at main deck prior to function test WL BOP and pressure test 7/32' rams on stump. Parallel activity: Cleaned pump rum and iron rough neck." "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Function tested WL BOP." "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Held tool box talk and pressure tested WL BOP on stump 20/345bars 5/10 mins." "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Continued preparing WL equipment prior to be spotted below cantilever and in Moon pool." "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.8 hours. Operational details: Continued preparing WL equipment prior to be spotted below cantilever and in Moon pool Parallel activity: Abseilers unable to work in derrick due to high winds" "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 9.2 hours. Operational details: Continued preparing WL equipment prior to be spotted on main deck and in Moon pool. Changed out WL drum from 7/32' braided wire to 7/32' E-line. Parallel activity: Rigged up work basket with various tools to assist Abseilers. Abseilers continued rigging up in preparation for alignment of FWD PRS, upper section of derrick." "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Continued preparing WL equipment prior to be spotted on main deck and in Moon pool. Parallel activity: Held tool box talk and performed line test from Cmt unit to drilling BOP F-15. Closed shear rams and bled of manifold hydraulic pressure, verified pos-lock keeping the blind/shear ram closed. Leak tested the well to 180 bars 10 mins against closed blind/shear. Abseilers continued to securing lifting gear to move PRS to vertical." "On 2008-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.0 hours. Operational details: Transferred weather deck hatch cover down to the welders store and cut a 350mm hole for the WL riser. Prepared WL equipment to be lowered into the Moon pool. Dismantled high pressure pipe on the drilling BOP to get access with the WL Lubricator. Parallel activity: Abseilers continued rigging up in preparation for alignment of FWD PRS, upper section of derrick. Lined up to read pressure on choke manifold, opened all HCR's on BOP, closed required manual valves, RIH donut and landed off on blind/shear ram, closed Upper rams with low pressure, adjusted donut and increased manifold pressure to activate locks on rams, reduced pressure on manifold." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Continued preparing WL equipment to be lowered down to the Moon pool. Parallel activity: Abseilers continued rigging up in preparation for alignment of FWD PRS, upper section of derrick." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Lowered WL equipment down into the Moon Pool including the modified hatch cover." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Shut in F-5. Commenced installation of the modified hatch cover." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Prepared to open main hatch to Moon pool. Lowered WL BOP and Grease injection pump into the Moon pool." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Started to spot WL equipment in the Moon Pool. Parallel activity: Held tool box talk and commenced to re-align FWD PRS as per SJA/ PLAN." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Electrician supplied power to Seawell wire line winch on main deck." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Prepared to open main hatch to Moon pool." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.8 hours. Operational details: Held tool box talk and started to rig up riser and WL BOP. Tested counter on WL winch and load cell. Parallel activity: Held tool box talk, continued to re-align FWD PRS as per SJA/Plan." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Filled riser/BOP prior to leak test. Lowered Seawell pump skid down into the Moon Pool." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Continued to spot and arrange Seawell WL equipment in the Moon Pool. Prepared for pressure test of WL riser and BOP. Parallel activity: Spotted additional lifting gear required in derrick, lift same to rig floor." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Pressure tested Seawell WL riser and BOP 20/345 bars 5/10mins. Parallel activity: Abseilers continued in derrick re-arranging the lifting equipment on FWD PRS." "On 2008-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Installed kill line and bled off line on KWV. Connected control line to the WL BOP. Parallel activity: Abseilers continued in derrick re-arranging the lifting equipment on FWD PRS. Cleaned in pump room and shakers." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Prepared GIH and checked tool catcher. Pulled cable up to Schlumberger work shop on main deck. Built Schlumberger cable head. Parallel activity: Abseilers continued in derrick re-arranging the lifting equipment on FWD PRS." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.8 hours. Operational details: Made up control lines to HMV and leak tested 210bars 10mins. Made up control line to DHSV and leak tested to 520 bars 10min. Parallel activity: Abseilers continued in derrick re-arranging the lifting equipment on FWD PRS. Held tool box talk/SJA in dog house with all involved personnel prior to re-align FWD PRS." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Started to make up lubricator in Moon Pool. Parallel activity: Started to re-align FWD PRS as per SJA/ PLAN." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Continued making up lubricator in Moon Pool." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Continued rig up equipment in the Moon Pool. Parallel activity: Held tool box talk with new crew & commenced to re-align FWD PRS as per SJA / PLAN." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.0 hours. Operational details: Continued rig up equipment in the Moon Pool. Rigged up lifting arrangement for the Lubricator. Parallel activity: FWD PRS now in vertical position. Secured & investigated upper shaft, & made forward plan." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Lowered gun into the Moon Pool. Continued making up lubricator. Parallel activity: Held tool box talk with Abseilers and Varco prior to inspection of PRS." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Rigged up air hoist for handling BHA. Made up Lubricator to the BOP. Parallel activity: Abseilers and Varco inspected the FWD PRS." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Pulled back the tool string into the tool catcher. Held tool box talk prior and leak tested lubricator 20/345 bars for 5/10min. Parallel activity: Abseilers and Varco inspected the FWD PRS." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held tool box talk prior to make up 3 3/8' guns." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Picked up 3 3/8' gun and found lifting heights not to be sufficient. Re-arranged Air hoist." "On 2008-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Picked up and landed of the 3 3/8' gun in the WL BOP." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Prepared firing head and made up same to the 3 3/8' gun." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Made up lubricator and leak tested In-SiTu connection to 345 bars. Pulled BHA up into the tool catcher." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Held tool box talk and opened HMV and applied 520 bars to the DHSV. Equalized across the DHSV with the Cmt unit pumping 100% MEG. DHSV opened at 33 bars SIWHP. Bled off surface lines." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: RIH with 3 3/8' gun from surface to 3420m. Parallel activity: Held tool box/SJA meeting prior to move the FWD PRS out into park position." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3640m. The activity was categorized as 'workover -- perforate' and lasted for 5.2 hours. Operational details: Continued RIH with perforating guns on WL from 3420m - 3640m. Stopped RIH and bled off WHP to approx. 1 bars. Parallel activity: Unable to work in derrick, due to high wind." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3624m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Correlated and positioned guns. Perforated interval from 3619m to 3622m." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: POOH with perforation gun from 3624m to surface." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: At surface closed the HMV, bled off pressure in the lub/riser and inflow tested HMV. Parallel activity: Climber up in derrick and evaluated rigging up to be able to move FWD PRS." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Broke lubricator and laid out 3 3/8' guns all shots fired. Parallel activity: Unable to work in derrick, due to high wind." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Made new firing head. Picked up new 3 3/8' guns and lowered into the BOP/riser and connected up to the firing head. Picked up BHA into the lubricator and found guns floated with water." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.2 hours. Operational details: Laid down 3 3/8' guns and picked up back-up with orientated weight made up. Lowered into the BOP/riser and made up guns to firing head." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Made up the In-SiTu sub and leak tested to 150bars 10 min. Line up to the Cmt unit and filled the riser/BOP/lub with 100 % MEG. Applied 11 bars and equalized across the XMT." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Opented XMT and RIH with 3 3/8' guns from surface to 300m." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Cleared and cleaned in the Moon Pool and weather deck. Built scaffolding walk way to get better access the WL lubricator platform." "On 2008-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1000m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Continued RIH with 3 3/8' guns from 300m to 1000m." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3420m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Continued RIH with 3 3/8' guns from 1000m to 3430m. Correlated across pup jnt at 3432m." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3660m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Continued RIH with 3 3/8' guns from 3430m to 3660m." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3610m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: Correlated across perforation depth and pup jnt at 3432m. Had to make 5 correlation passes due to stretch in the 7/32' E-line. Perforated interval from 3605m to 3608m. SIWHP 6 bars dropped to 5 bars and picked up to 6 bars immediately when guns fired." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 1250m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: POOH with 3 3/8' guns from 3610m to 1250m" "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: POOH with 3 3/8' guns from 1250m to surface." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held tool box talk prior to disconnect the lubricator and lay out the 3 3/8' guns." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Inflow tested HMV and disconnected WL lubricator. Laid out 3 3/8' guns. All shots fired. Installed XMT cap on top of the WL BOP and leak tested same to 20/345bars 5/10 mins. Parallel activity: Held tool box talk and moved FWD PRS to 1 meter from FWD sea fastening." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Held tool box talk prior to leak test KWV and Swab. Checked line up for leak testing of KWV and Swab valve. Parallel activity: Repaired chain pull in derrick and continued to move FWD PRS to FWD position." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Leak tested KWV and Swab valve 35/345bars 5/10 mins." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Maersk production established control of HMV and DHSV CL." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.5 hours. Operational details: Started water injection in F-5. Parallel activity: Continued to move PRS to FWD position." "On 2008-10-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.0 hours. Operational details: Continued water injection in F-5. 9000m³/day 172 bars. Parallel activity: Inspected derrick. Assessed PRS beam lift points. Prepared scaffolding on deck. Climbers carried out full PRS visual check. Spotted scaffolding on rig floor. Prepared and spotted PRS parts on cantilever. Sea fasted FWD PRS." "On 2008-10-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Continued water injection in F-5. 8700m³/day 160 bars. Parallel activity: Prepared equipment/scaffolding for hoisting up in derrick. Hoisted and erected scaffolding in derrick around FWD PRS at upper drive." "On 2008-10-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 11.5 hours. Operational details: Continued water injection in F-5. Meanwhile: Pressure tested CRI hose to 200 bar/10 min." "On 2008-10-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Production prepared well prior to RD WL, due to low WHP, function tested DHSV. Meanwhile held tool box talk prior to commence RD WL." "On 2008-10-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Started to RD WL. Cut wire and laid down Cable head and Cal-B. Spooled back wire to the WL winch. RD GIH and Lubricator." "On 2008-10-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: RD WL BOP and riser. RD chiksan on KWV and installed blind cap. Leak tested tree body to 35/380 bar 5/10 min. Opened Swab and KWV and leak tested KWV, blind cap, HMV and XMT cap 35/380bars 5/10 mins. RD test line and placed hole cover." "On 2008-10-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Handed well over to production." "On 2008-10-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.8 hours. Operational details: Continued RD WL surface equipment." "On 2008-10-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 9.8 hours. Operational details: RD WL surface equipment. Changed drum in WL winch. Cleared and cleaned area. Removed scaffolding from Moon Pool. RD Schlumberger cable on cantilever." "On 2012-09-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Well handed over from production department. Held brief prior to leaktest XMT cross." "On 2012-09-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Found out that DHSV was open. Closed DHSV and bleed down pressure above to closed drain." "On 2012-09-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Leak tested XMT cross to 20/120 bar for 5/10 min." "On 2012-09-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Skidded rig in position." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Changed to workover hatch." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Held DOP meeting on drill floor prior to R/U on well." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Removed XMT top cap and installed lower riser and BOP. Installed chiksan manifold on KWV." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Leak tested lower riser/BOP connections to 20/120 bar for 5/10 min and function tested BOP. Leak tested chiksan manifold against closed KWV to 20/120 bar for 5/10 min." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Lowered down lower lubricator from rig floor and stabbed onto BOP." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed debrief." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Lifted up lubricator and GIH in elevator. Add appox 40 litres of Ramex RX 72 into riser." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Installed RST toolstring into lubricator." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Continued to install RST toolstring." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.6 hours. Operational details: Made up connections and filled lubricator with MEG. Tested R/U to 20/120 bar for 5/10 min." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3645m. The activity was categorized as 'workover -- wire line' and lasted for 3.6 hours. Operational details: Opened well and RIH with BHA#1, RST toolstring to 3645 m. WHP: 42 bar" "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3642m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Ran correlation pass between 3645 and 3420 m. Adjusted the depth according to reference log." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3456m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Logged RST-D in Sigma mode between 3642 - 3456 m @ 4.5m/min." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3635m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: RIH from 3456 to 3642." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3460m. The activity was categorized as 'workover -- wire line' and lasted for 7.1 hours. Operational details: Logged RST-D in IC mode pass#1 from 3635 - 3460m @ 0.5m/min." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3637m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH from 3460 to 3637." "On 2012-09-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3600m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Logged RST-D in IC mode pass#2 from 3637 - 3600 m @ 0.5m/min." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3460m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Logged RST-D in IC mode pass#2 from 3600 - 3460 m @ 0.5m/min. WHP: 42 bar." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3637m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: RIH to 3637 m." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3460m. The activity was categorized as 'workover -- wire line' and lasted for 9.6 hours. Operational details: Logged RST-D in IC mode pass#3 from 3637 - 3460 m @ 0.5m/min. WHP: 42 bar." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: POOH with BHA#1 from 3460 m to surface." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: OOH. WHP 42 bar. Closed well and inflow tested HMV and SV." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.7 hours. Operational details: Closed DHSV and bled down to 10 bar. Inflow tested DHSV. Bled off pressure above and closed well. Meanwhile held DOP meeting prior to R/D." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Had problem to flush lubricator with N2 through manifold on KWV to blow down. Found rubber particles in LTV. Removed rubber and continued to flush lubricator with N2." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Broke lubricator and L/D BHA#1 on drill floor. Inspected same." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held brief prior to R/D upper lubricator and GIH." "On 2012-09-17, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: R/D upper lubricator, GIH and hoses. Disassambled lubricator and lifted out lubricator from rig floor." "On 2012-09-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Held brief prior to R/D lower lubricator and BOP." "On 2012-09-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.1 hours. Operational details: Lifted lower lubricator to rig floor with top drive. Lifted BOP away in moon pool. RD lower riser. Installed tree cap. R/D manifold on KWV. Installed KWV cap. Lifted out grease pump and N2 bottles from rig floor. Lifted out BOP from moon pool." "On 2012-09-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.2 hours. Operational details: Lined up and leak tested XMT cross to 20/280 bar for 5/10 min. Leak tested tree cap and KWV cap to 20/345 bar for 5/10 min." "On 2012-09-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.0 hours. Operational details: Continued to rig down WL equipment. Handed well back to production." "On 2012-09-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Packed and prepared for back load. **********End of operation.***************" "On 2015-11-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Skid rig from F-11 B to F-5." "On 2015-11-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Changed 7/16' add-on drum, due to cable strands outside criteria for building new cable head. Meanwhile received well from production." "On 2015-11-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: Had to wait for rigging on XMT due to leak in header valve on water injection line. Meanwhile rigged up new add-on drum and changed to wireline hatch." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: Waited on production department to isolate injection line. Meanwhile rigged up new add on drum." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.2 hours. Operational details: Rigged up KWV manifold. Inflow tested swab valve to 140 bar for 10 min. Leak tested KWV manifold to 20/140 bar for 5/10 min. Meanwhile built new GIH and threaded cable. Schlumberger built cable head and tested toolstring." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to disconnect XMT cap and land riser, BOP and lubricator." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Disconnected XMT top cap and Landed riser, BOP and Lubricator. Hooked up hoses for the BOP. Meanwhile Schlumberger tested BHA on deck." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Function tested BOP and leak tested bleed off hoses on wellhead to 20/140 bar for 5/10 min." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Prepared for lifting lubricator." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting on rig floor prior to lift up lubricator and perform RST logging." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Lifted lubricator into vertical position. MU QTS to riser." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: M/U BHA # 1 2,51' RST-D. M/U lubricator to QTS." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.4 hours. Operational details: Fill RU with 100% MEG. Leak tested lubricator/QTS/riser against SV to 20/200 bar 5/10 min." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.3 hours. Operational details: Waited on Production for pumping and equalizing pressure over DHSV." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Opened HMV and equalized pressure above DHSV, applied 430 bar on CL to DHSV. WHP 57 bar when DHSV equalized. Opened SV." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 383m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH w/ BHA # 1 2,51' OD RST-D from surface m to 383m, WHP 57 bar." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 383m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Schlumberger checked communication with logging tool." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3630m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Continued to RIH from 383 m to 3630 m. Depth P/U 2000 m 2600 lbs 2400 m 3150 lbs 3000 m 3900 lbs 3200 m 4300 lbs 3600 m 4500 lbs Friction factor 0,22." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Logged RST-D Sigma pass at 4,5 m/min across interval 3625 - 3450 m. WHP 56 bar." "On 2015-11-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 6.9 hours. Operational details: RIH to perform RST-D IC pass at 0,5 m/min across interval 3525 - 3470 m . Performed three passes. Meanwhile interpreted logging data. Decided to run a fourth pass while interpretating. WHP 54 bar." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3470m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Logged fourth RST-D IC pass across interval 3525 - 3470 m. Completed logging." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.6 hours. Operational details: POOH from 3470 m to surface . WHP bar. 54 bar." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.4 hours. Operational details: Closed SV & HMV and inflow tested same. Purged lubricator with N2. Observed grease in bleed off hose." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Found empty container to drain grease, to avoid getting same into bleed-off lines." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Continued to purge lubricator." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to L/D BHA#1." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Broke lubricator and L/D BHA on deck." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Rigged down top lubricator and prepared for rigging down lubricator." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.2 hours. Operational details: Closed BOP and opened HMV. Bled off pressure above DHSV and inflow tested same, 0,03 bar/30 min." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.8 hours. Operational details: Opened BOP. Rigged down lubricator and L/D on drill floor. Disconnected hoses to BOP. Lifted BOP and placed same in moonpool. Meanwhile Schlumberger rigged down logging unit." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.7 hours. Operational details: Disconnected lower riser section and L/D same on drill floor. Installed top cap. Disconnected KWV manifold and installed KWV cap." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.6 hours. Operational details: Leak tested top cap and KWV cap to 20/345 bar for 5/10 min." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Disconnected hoses to XMT HMV and DHSV. Cleaned and tidy area. Handed well over to production department." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Lifted lubricators into containers and rigged down equipment on pipedeck. Lifted BOP from moonpool into container on pipedeck." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Reeled back HMV & DHSV and packed skid. Packed BOP pressure control skid." "On 2015-11-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Packed chicksan container and removed scaffolding around wireline winch." "On 2015-11-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Packed wireline winch and 7/16' add-on." "On 2015-11-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Packed Altus work container. Cleaned and tidy area. ----------------------- END OF OPERATION ----------------------" "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.0 hours. Operational details: Skidded rig from F-11 to F-5" "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Handover meeting of well from production department to Intervention." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Changed permanent hatch with WL hatch." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Rigged up chiksan manifold to KWV. Leak tested same to 20/345 bar for 5/10 min. Removed Top cap on XMT." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk before lifting Riser section and BOP to XMT." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Lifted and installed riser section and BOP from moonpool area to XMT." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Connected Altus pump and hoses for local control of DHSV and HMV." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Lifted lubricator and GIH from catwalk and hung off above riser section on drill floor." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held toolbox meeting prior to installing BHA #1 (572-700 ME plug) in lubricator." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.8 hours. Operational details: M/U BHA for run #1 (572-700 ME plug). Leak tested lubricator to 20/345 bar 5/10 min." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.4 hours. Operational details: Equalized and opened HMV and DHSV. WHP = 45 bar" "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 278m. The activity was categorized as 'workover -- other' and lasted for 0.6 hours. Operational details: Opened SV and RIH with BHA #1 (572-700 ME plug) to 278 mMD. Schlumberger checked tools." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3630m. The activity was categorized as 'workover -- other' and lasted for 2.8 hours. Operational details: RIH and observed BHA starting to float. Reduced speed to 20 m/min and continue to RIH to 3630 mMD. Took PUW every 500 m. Depth (m) PUW (Lbs) 500 1310 1000 1830 1500 2490 2000 3020 2500 3780 3000 4600 3500 5450 Actual Friction factor: 0,3." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3630m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Performed correlation passes prior to installing plug. Observed some problems while correlating due to stick slip on BHA." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3592m. The activity was categorized as 'workover -- other' and lasted for 0.4 hours. Operational details: Positioned and installed plug with mid packer element at 3592 mMD. Lost 300 lbs on tension during installation. WHP before/after setting 45 / 45 bar." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: POOH from 3592 m to surface . WHP decreased from 45 bar to 2,4 bar while POOH." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.3 hours. Operational details: Attempted to leak test XMT. Unable due to leakage. Most likely in PWV." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Pressured up tubing to 50 bar to inflow test SV and HMV." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.4 hours. Operational details: Closed and inflow tested HMV and SV." "On 2016-04-18, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.6 hours. Operational details: Bled down tubing pressure to 5 bar. Inflow tested ME plug to 45 bar dP for 30 min. Pressure increased 0,15 bar / 30 min" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Purged Lubricator with N2." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Held toolbox talk prior to L/D BHA #1." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.7 hours. Operational details: Broke lubricator and L/D BHA #1 on deck. Checked and verified setting tool OK." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Schlumberger tested cable head." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to M/U BHA #2 (Perforation guns)" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Lifted BHA up to drill deck using rig crane." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.6 hours. Operational details: M/U BHA for run #2 (Perforation guns). Leak tested QTS to 20/160 bar 5/10 min." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Opened SV and HMV. WHP = 0 bar." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 600m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: RIH w/ run #2 (Perforation guns), 4 1/2' OD guns to 600 m." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 600m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Schlumberger powered up and checked tools at 600 m" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3550m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Continued to RIH with BHA #2 from 600 m to 3550 m. Took PUW every 500 m Depth (m) PUW(lbs) 500 2250 1000 2850 1500 3540 2000 4050 2500 4800 3000 5400 3500 6100 Actual friction factor: 0,18" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3550m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Performed 4 correlation passes interval 3460 m to 3550 m." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3510m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: P/U and placed bottom shot at 3510 m and top shot at 3501 m. Bled off WHP to 3 bar, took some time to bleed off." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3510m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Perforated well interval 3501-3510 m. Lost 170 lbs on tension. WHP before/after 3/12,2 bar , A-Annulus before/after 12,8/12,8 bar, B-annulus before after 7,2/7,2 bar" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3460m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Logged CCL up from shooting depth to 3460m." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.2 hours. Operational details: Continued POOH to surface. WHP = 11,9 bar." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Closed HMV and SV. Inflow tested SV by pressuring up XMT to 200 bar." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Purged lubricator with N2." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to L/D perforation BHA." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Broke lubricator. L/D BHA on deck. Confirmed all shots fired." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.2 hours. Operational details: Schlumberger tested tools for next run with BHA #3 (Perforation guns)." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to R/U BHA #3 (Perforation guns)" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.5 hours. Operational details: M/U BHA for run #3 (Perforation guns). Stabbed lubricator and leak tested QTS to 20/160 bar 5/10 min." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Equalized and opened SV and HMV. WHP = 13,5 bar." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 600m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: RIH w/ run #3 (Perforation guns), 4 1/2' OD guns from surface to 600 m." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 600m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Schlumberger powered up and checked tools at 600 m" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3550m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: Continued to RIH with BHA #3 from 600 m to 3550 m. Took PUW every 500m. Depth (m) PUW (lbs) 500 2400 1000 3100 1500 3850 2000 4400 2500 5100 3000 5800 3500 6250 Actual friction factor: 0,18" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3507m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Performed 5 correlation passes across interval 3430 m - 3507 m." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3492m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: P/U and placed bottom shot at 3492 m and top shot at 3474 m." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3492m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Perforated well interval 3474-3492 m. Lost 380 lbs on tension. WHP before/after 12,8/8,6 bar , A-Annulus before/after 12,7/12,7 bar, B-annulus before after 7,2/7,2 bar." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 3430m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Logged CCL up from shooting depth to 3430m." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.7 hours. Operational details: POOH from 3430 m to surface. WHP: 9 bar" "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Closed HMV and SV." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Purged lubricator with N2. Had to open SV and take return through XMT due to 'grey grease' liquid in lubricator." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Closed and inflow tested SV and HMV." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to L/D perforation BHA." "On 2016-04-19, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Broke lubricator to L/D BHA #3." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: L/D BHA #3 on deck. Confirmed all shots fired." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: M/U dummy BHA for testing lubricator. Installed and stabbed lubricator. Leak tested QTS in lubricator to 20/160 bar for 5/10 min" "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Closed DHSV and opened HMV. Bled down pressure in tubing from 9 bar to 1 bar." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.8 hours. Operational details: Inflow tested DHSV to 8 bar dP for 30 min. Pressure increased 0,27 bar / 30 min." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to L/D Lubricator and GIH to catwalk." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Closed HMV. Broke lubricator and L/D Dummy BHA." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: L/D Lubricator and GIH on catwalk using rig-crane and top drive." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Stabbed on lifting sub to riser section. Unable to latch with drilling elevator due to hydraulic leakage." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Waited for mechanic to fix hydraulic leakage in drilling elevator. Meanwhile, leak tested KWV to 20/345 bar for 5/10 min." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Disconnected lower riser from XMT. Liftet entire riser section and BOP from XMT up to moonpool area." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Installed top cap on XMT. Tested same to 20/345 bar for 5/10 min." "On 2016-04-20, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Handed well over from Intervention to Production department. ------------------------ End of Operation ----------------------" "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding cantilever to F-5." "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Prepared and skidded rig 3m port and 2m aft." "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew" "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Prepared to continue skidding rig. Noticed cantilever in correct position to swap hatches on F-7 and F-9 (for upcoming future operations on F-9)." "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for swapping hatches on F-7 and F-9. Meanwhile: Worked on flow line cover." "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.2 hours. Operational details: Swapped hatches on well F-7 and F-9. Meanwhile: Worked on flow line cover." "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded cantilever to well F-5" "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Installed stairs to access cantilever." "On 2016-08-28, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Removed hatch on F-5 and installed half moon hatches. Meanwhile: Opened doors on BOP. Worked on flow line cover/goose neck." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Continued to remove hatch on F-5" "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U cement spool" "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: R/U cement spool to XT" "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U chiksan and hoses to cement spool. Installed half moon hatches Meanwhile: Pressure tested cement unit." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Built scaffolding around cement spool and BOP stump. Continued working on BOP, opened up rams for inspection/cleaning. Found minor traces of cement and swarf. Meanwhile: Performed post-skid checks and housekeeping in drilling areas. Short change of drilling crew at 0400." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued building scaffolding around cement spool and BOP stump. Continued working on BOP, cleaning. Meanwhile: Continued post-skid checks and housekeeping." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Connected cement spool bleed-off hose. Continued working on BOP. Meanwhile: Performed post-skid checks, housekeeping and dailys." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Build scaffolding hand rails and stairs for safe access to hatch deck. Meanwhile: Continued working on BOP, performed post-skid checks and housekeeping." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing cement spool" "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continue building scaffolding hand rails and stairs for safe access to hatch deck. Meanwhile: Continued working on BOP, performed post-skid checks and housekeeping." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lined up and flushed lines to cement spool. Pressure tested cement spool to 20/335 bar for 5/10 min. Bled off pressure to closed drain." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lined up and attempted pressure tested kill wing manifold 20/335 bar. Leaking hose between kill manifold and cement spool." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Replaced leaking hose." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pressure tested kill wing manifold to 20/335 for 5/10 min." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for bullheading SW" "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Opened HMV, 7 bar trapped below. Bled off pressure in well to 1,3 bar through closed drain." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.2 hours. Operational details: Opened SV and trapped 10 bar behind LTV 7 on cmt spool. Opened LTV 7 and observed pressure drop, correct line up. Pressured up control line for DHSV to 520 bar. Bullheaded 3 m3 50/50 MEG/SW followed by 10 m3 wash pill at 200-400 lpm. DHSV equalized at 54 bar after 8 m3 pumped. Lined over to SW, and bullheaded SW at 1300 lpm. Observed pressure increasing to 305 bar after 76 m3 of SW pumped. Decreased flow to 1000 lpm, pressure decreased and stabilized at +/- 245 bar. Increased flow in steps to 1300 lpm / 273 bar. Continued bullheading 182 m3 SW at 1300 lpm, pressure decreased and stabilized at 1300 lpm / 250 bar. Totally pumped 258 m2 of SW. Meanwhile: Performed TBT for cement job." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Shut down pumps and lined up to cement unit." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Closed LTV 7 and opened LTV 9. Released bottom dart. Mixed and pumped 12,3m3 1,90sg cement slurry at 600 lpm / 175 bar. Displaced surface lines with 0,9m3 hi-vis pill from cement unit. Released top dart. Closed LTV 9 and opened LTV 11. Continued pumping 13,7m3 hi-vis pill from cement unit at 600 lpm / 150 bar. Opened LTV 7 and LTV 9. Pumped 38,3 m3 SW at 1300 lpm / 194 bar from cement unit. Cycled DHSV 3x times after 30 m3 SW pumped. Pumped 4,3m3 contamination pill from cement unit at 700 lpm / 160 bar. Final squeeze pressure 208 bar. Final static pressure 96 bar. Stopped pumping. Estimated TOC at 2949 mMD." "On 2016-08-29, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: WOC Closed SV and bled off pressure in cement spool to closed drain. Meanwhile: Monitored pressure in XT cross from control room." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: WOC Inspected and prepared BOP for pressure testing. Meanwhile: Monitored pressure in XT cross from control room. Bled off pressure in XT cross from 133 bar to 96 bar." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: WOC Continued inspection of BOP. Prepared for pressure testing BOP and manifold. Unable to achieve pressure test of cement unit. Meanwhile: Monitored pressure in XT cross from control room. Bled off pressure in XT cross from 133 bar to 96 bar. Started to change out PRS wires." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: WOC N/U NT2 connector on BOP. Troubleshot leak on cement unit. Meanwhile: Monitored pressure in XT cross from control room. Bled off pressure in XT cross from 137 bar to 96 bar. Continued changing PRS wires." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: WOC Prepared BOP test mandrel. Performed TBT for BOP test. Started BOP test. Pressure tested kill manifold to 20/345 bar for 5/10 min. Lined up and flushed BOP. Meanwhile: Monitored pressure in XT cross from control room. Bled off pressure in XT cross from 136 bar to 96 bar" "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: WOC Pressure tested LPR to 20/345 bar for 5/10 min with SW." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: WOC Performed TBT for pressure testing BOP with onging crew. Continued BOP test." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing and inflow testing cement plug" "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Closed HMV and bled off pressure between SV and HMV to closed drain. Opened SV and equalized pressure above HMV Opened HMV and increase pressure to 315 bar Closed SV and bled off pressure above SV" "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Attempted to pressure test cement plug to 315 bar for 10 min. Monitored pressure in XT cross from control room. Increasing pressure trend. Meanwhile: Continued pressure testing BOP." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Bled down pressure to 80 bar to closed drain. Observed pressure for 5 min. Continued bleeding down pressure in 10 bar increments to 10 bar. Meanwhile: Continued BOP test." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Inflow tested cement plug to 15 bar differential pressure for 30 min. Meanwhile: Continued BOP test." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lined up and equalized above SV. Opened SV and pressure tested cement plug to 315 bar for 10 min. Meanwhile: Opened BOP and removed test mandrel." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Closed DHSV and bled down pressure to 240 bar above. Performed low pressure inflow test of DHSV to 70 bar / 30 min Bled down pressure above DHSV to 10 bar. Performed hi-pressure inflow test of DHSV to 305 bar / 30 min." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Pressured up to 315 bar to equalize pressure above DHSV. Opened DHSV and bled down pressure in well to 20 bar. Closed DHSV. Bled off all pressure above DHSV. Closed SV. Opedned SV and confirmed no pressure build-up. Drained cement spool and closed SV. Meanwhile: Performed TBT for R/D cement spool" "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Disconnected hoses and removed gauges from cement spool" "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed XT instrumentation. Meanwhile: BOP POD. Disconnected BOP NT2 connector from stump. Pressure tested manifolds." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued R/D cement spool. Removed scaffolding. Meanwhile: Pressure tested manifolds." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/D cement spool with ongoing crew." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Checked all lifting equipment for lifting cement spool." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Lifted cement spool and L/D in moonpool." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U and attempted to install BPV plug Plug not catching onto threads, possibly due to dirt in TH area." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Pulled out with BPV plug and inspected same. Threads in good condition, and no damages on the plug. Re-attempted several times to install plug." "On 2016-08-30, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Left BPV plug loose in the TH to act as junk catcher for the DHSV." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed chiksan hoses and control lines from WH/XT." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Removed hatches on F-5 and F-10. Removed beam between wells." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed elevator from bails. Installed lifting chains to TDS." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled master bushing and rotary ring. Installed handrail around rotary. Meanwhile: Performed TBT for lifting XT." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lowered lifting equipment from rotary down to moonpool. Attached lifting equipment to XT." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed XT clamp" "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Lifted XT into moonpool and landed on skid." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Secured XT on skid." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lowered tuggers down to WH deck. Attached spacer spool to lifting arrangement. Lifted spacer spool from WH deck to drill floor. L/D spacer spool. M/U BPV plug in TH. Observed dirt in the TH area." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed master bushing. Confirmed no pressure in WH voids. Disconnected control lines on WH and blinded off ports. Meanwhile: Installed mouse hole and L/O RT. P/U HP riser joint." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installing communication collar. Meanwhile: Measured distance RKB - WH 20,0 m." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed communication collar. Meanwhile: Lifted XT from moonpool to main deck. Performed TBT for installing hatches." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Installed beam and hatch on F-10." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for running HP riser joint." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Ran HP riser joint and set down 2 ton. M/U connector on WH." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed split hatch around riser joint." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Built scaffolding around riser joint. Meanwhile: Prepared for running slick joint and diverter. Performed TBT for N/U BOP/Diverter." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Skidded BOP from test stump to well center. Landed BOP on NT-2 connector." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Built remaining scaffolding around riser joint." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed slick joint." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Installed tension cylinders. Starboard aft and fwd tension cylinders misaligned to the BOP. Meanwhile: M/U BOP NT-2 connector to riser." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Load shifted weight from BOP carrier to tension system." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Ran diverter 0,1 m above slick joint. Aligned slick joint/BOP to diverter using tension system and BOP carrier. Landed diverter and disconnected lifting equipment. M/U slick joint." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for working on the slick joint." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed master bushing. R/D diverter RT." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: N/U slick joint nuts. N/U overshot. Meanwhile: Prepared tubing handling equipment on drill floor. Liftet casing tong to drill floor. Prepared BPV RT BHA." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: De-isolated and pressured up BOP control system. Meanwhile: R/U chiksan hoses on WH. Performed TBT for connector test." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lined up and filled BOP. Performed BOP connector test to 20/345 bar for 5/10 min. Meanwhile: Continued R/U of chiksan hoses on WH." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: RIH with BPV RT on 3 1/2' DP. Latched onto dart and POOH and L/D. Meanwhile: Continued R/U of chiksan hoses on WH." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: RIH with stinger BHA. Pulled BPV plug. POOH and L/D tools. Meanwhile: Continued R/U of chiksan hoses on WH." "On 2016-08-31, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Prepared and R/U casing tong." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued R/U casing tong. Changed inserts in elevator. Meanwhile: Continued R/U chiksan hoses on WH. Performed TBT for M/U THRT" "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Prepared control line spool for THRT." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U and M/U THRT. Spaced out for BOP. Meanwhile: Contiued R/U hoses on WH." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U control lines to THRT." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with THRT on 7' landing string to 19.9m. Latched onto TH. Pulled 10 ton overpull to confirm latch." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and attempted to M/U 7' swedge. Too small OD on swedge for casing tong to M/U. Meanwhile: Performed line test of hoses on WH." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: P/U and M/U circulation swedge. Meanwhile: Continued line test on WH." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U cement hose and lo-torque valve." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed line-up test to circulatoin swedge. Pressure tested cement hose to 100 bar for 10 min." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lined up to rig pumps. Pressured up DHSV control line to 520 bar. Pressured up tubing to 90 bar, indication of DHSV opened on control line pump. Bled off and monitored for pressure build-up in tubing for 5 min. No pressure build-up observed." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cement hose and B/O circulation swedge." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U WL" "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U wireline equipment." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U WL equipment. Observed crude oil dripping out of tubing while R/U WL, 0,5 ltrs/min. Installed swedge. Flowchecked well and monitored annulus gauge for 30 min, static. Meanwhile: Performed TBT for M/U cutter toolstring." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U cutter toolstring" "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: RIH w/ cutter toolstring from surface to 2800 m." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Correlated depth and positioned cutter at 2774 mMD." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressure tested surface lines to 20/345 bar for 5/10 min." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up to monitor pressure on annulus while performing cut. Cut tubing at 2774 mMD, good indications of cut, lost 280 lbs weight. No change in pressure observed on annulus." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: POOH from 2774 m to surface." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D toolstring." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D wireline equipment." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U swedge and installed cement hose. Lined up to circulate over poor boy degasser." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for handling H2S and gas on surface and pump room." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Circulated 2 x B/U down tubing and returns through choke via poor boy degasser, 1300 lpm / 130 bar. Max gas 6,2%, 1 ppm H2S in gas trap." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Flowchecked well, observed backflow out tubing 1 lpm. Backflow decreased and stopped. R/D swedge. Meanwhile: Performed TBT for releasing, pulling and L/D tubing hanger." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Released TH. Attempted to pull TH, 130 ton overpull. Worked string up/down several times." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Worked string up/down. Max hookload 287 ton. Monitored well on TT, static. Nautral weight (tubing weight + block weight) 158 ton. Strech measured from 158 ton to 287 ton, 6 cm. Estimated stuck point 55m. Most likely TH stuck at 20m." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for investigating stuck tubing" "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Closed A-annulus valves and removed hose on annulus outlet. Opened valves, no backflow observed. P/U to 280 ton and slacked off to 67 ton, repeated 3 times. Noticed multibowl moving when picking up weight." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation. Meanwhile: Filled riser, monitored well on TT, static. Closed DHSV." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Rotated 8 turns right hand to release communication collar. Worked string up/down 157/67 ton hookload (92 ton OP). THRT came free at 157 ton hookload." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with THRT and L/D same." "On 2016-09-01, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed hoses on WH. Installed new pressure gauge on annulus outlet on WH. Meanwhile: Inspected diverter and drilling equipment after movement." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Evaluating situation. Meanwhile: Performed maintenance and housekeeping" "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for running spear and pack-off." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U spear assy with pack-off." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Inspected and serviced spear and grapple." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH with spear to 25,1m. Enganged spear. Attempted to pull free TH with 30 ton overpull. Observed WH moving. Disengaged spear." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with spear assembly and racked back." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: Evaluated situation. Lined up to monitor well on TT and annulus gauge. Meanwhile: Serviced drilling equipment. Performed housekeeping in moonpool." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation Meanwhile: Moved casing tong to fox hole. Pressure tested stand pipe and choke manifolds to 20/345 bar for 5/10min. Prepared for slip&cut." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation Meanwhile: Performed slip&cut." "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation Meanwhile: Calibrated drawworks" "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 6.8 hours. Operational details: Waited on brine prior displacing well to heavy fluid Meanwhile: - Discussed with onshore organization. - Greased valves on choke manifold. - Serviced FWD PRS upper head rollers. - Performed housekeeping - Calibrated block weight sensor (mudlogger sensor)" "On 2016-09-02, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 5.0 hours. Operational details: Waited on brine prior displacing well to heavy fluid Meanwhile: - Prepared temporary trip tank - Serviced FWD PRS - Performed housekeeping - Cleaned pits - Prepared tools and equipment for N/D BOP" "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: Waited on brine prior displacing well to heavy fluid Meanwhile: - Continued servicing FWR PRS - Cleaned pits - Performed PMs" "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Waited on brine prior displacing well to heavy fluid Meanwhile: - Performed housekeeping - Worked on modification on encoder on drawworks. - Cleaned pits - Performed PMs" "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 6.5 hours. Operational details: Prepared for displacing well to brine. Cleaned pits (entering tanks) Meanwhile: - Performed PMs. - Performed housekeeping - Worked on drawworks - Prepared permits - Inspected TDS and TDS hoses - Tested BX3 elevator and rotator - Finished recieving brine from boat 13:30." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Prepared for displacing well to brine. Mixed 1.19sg CaCl2 brine and kill pill. Experienced foaming and lost suction from pit." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Flushed lines several times." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Prepared to displace well to brine. Mixed new kill pill. Meanwhile: - Removed slick joint nut (left 4 in)" "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with spear/grapple/pack-off assy to 26m and engage spear." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TBT for displacing well" "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Checked and confirmed line up. Walked the lines." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed new TBT due to uncerntainty in operation. Confirmed line-up." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Staged up rig pumps and pumped 37,2m3 1,19sg CaCl2 brine at 1200 lpm / 156 bar. Lined up and pumped 10m3 1,19sg CaCl2 kill pill. Pumped 48,2m3 1,19sg CaCl2 brine at 1200 lpm. Pressure started to increase, then dropped again before increasing to ~160 bar." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flow checked well through open choke. Some backflow observed, then static. Continued monitoring well on trip tank." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Disenganged spear and pulled pack-off out of tubing. Displaced BOP to 1,19sg CaCl2 brine." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Disconnected TDS. POOH with BHA. Checked tools and R/B BHA." "On 2016-09-03, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Rigged up to drain riser through A-annulus outlet on WH (u-tubing down tubing and returns through A-annulus)." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Drained riser. Meanwhile: Prepared BPV plug and running tool. Changed to 3 1/2' handling equipment." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Rigged up modified trip tank on WH deck. Attempted to flowcheck well on modified trip tank from A-annulus. Unable to pump or getting returns. Rigged up new pump. Re-attempted to flowcheck well on modified trip tank. Found VR plug blinded off service wing on WH." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Discussed situation." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for removing flange on WH." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed flange on WH. Removed VR plug. Re-installed flange on WH. Installed circulation valves for modified trip tank." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Performed extended flow check of well over modified trip tank on WH. Well static for 45 min, then losses. Lost 130 ltr/hr for 15 min. Observed small gain (20 ltrs), then static." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued flow checking well for 1 hr over modified trip tank on WH deck, static." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH and installed BPV plug" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with BPV RT. L/D same." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling diverter" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Prepared chains and lifting bridle for diverter. Pulled diverter" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled slip joint" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Load shifted to BOP carrier. Removed tension cylinders" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: N/D BOP" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed parts of scaffolding around riser to be able to skid over to test stump." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Moved BOP from well center to BOP test stump." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed remaining scaffolding around riser." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling riser." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed master bushing and outer ring. Attached chains and lifting bridle to riser joint. Disconnected riser from WH. Removed hole cover and pulled riser joint to drill floor. Installed outer ring and master bushing. Installed hole cover." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Inspected tubing hanger. Observed increased u-tube from well while removing communication collar." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installing riser" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Pulled master bushing and outer ring. Installed Riser." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Built scaffolding around riser joint" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Moved BOP from stump to well center. Landed BOP on riser joint." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Finished scaffolding around riser." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U NT-2 connector." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed tension cylinders. Load shifted weight from BOP carrier to tension system." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed slip joint" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed diverter. M/U slip joint" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for BOP connector test" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D chains from TDS. Installed BX elevator. Change to 3 1/2' inserts." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: M/U BPV RT. RIH to 6m." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U bolts on slip joint" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressureized diverter system and overshot packer." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Consulted onshore organization. Observed well on TT and modified TT on WH. Gained 240 ltr/20min at TT, lost 200 ltrs/20min on WH TT." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Consulted onshore organization. Well control duty and onshore organization concluded to perform BOP connector test and circulate well to even brine weight, no kill pill. Observed well on TT and modified TT on WH. Gained 140 ltr/20min at TT, lost 130 ltrs/20min on WH TT." "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with BPV dart RT to 20m. Installed dart. POOH" "On 2016-09-04, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up for connector test Meanwhile: Flushed TT with clean brine" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued line-up for connector test. Meanwhile: Flushed TT with clean brine." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed low pressure test of BOP connector, 20bar/5min. Continued pressuring up to 250 bar. Stopped pumping and checked that volume pumped corresponded with expected theoretical volume. Continued pressuring up to 345 bar. Performed high pressure test of BOP connector, 345bar/10min." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Retrieved BPV dart and BPV plug. Found chunks of cement on top of RT." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Canged to 5 1/2' handling equipment. Meanwhile: Performed TBT for RIH with spear and pack-off" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U spear/pack-off assy. Inspected tools." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with spear BHA to 26m." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Engaged spear and pulled 10 ton OP." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up to pump down drill string, taking returns through A-annulus via choke and poor boy." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Initiated circulation. SPP increased rappidly to 30 bar, no pressure on annulus gauge. Pumped slowly until pressure dropped from 63 bar to 7 bar. Observed returns on shaker." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Staged up pumps in steps to 1200 lpm / 144 bar. Return brine weight 1.18sg until 68 m3 pumped. At 68 m3 pumped the return brine weight decreased to 1.14sg and slightly changed color (kill pill with graphite). Return brine weight gradually increased to 1.17sg at 73 m3 pumped. At 77 m3 the return brine weight was back at 1.18sg. Circulated totally 118m3, until even brine weight in/out." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Stopped pumps. Disengaged spear. POOH with spear/pack-off BHA." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Flow checked well, static" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lined up to modified TT Monitored well on rig TT and modified TT. Observed expected u-tube down string and out of A-annulus (due to height difference of approximately 25m)." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Monitored well on rig TT only. Took sample from A-annulus, 15 ppm oil content. Meanwhile: Changed handling equipment. Prepared to N/D BOP and diverter." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Drained BOP and riser out A-annulus." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Monitored well on WH TT. Gained 50 ltrs first 30min, decreasing trend." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Monitored well on WH TT, static. Meanwhile: Installed BPV plug." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed handling equipment for pulling diverter." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed bolts on slipjoint" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/D BOP" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled master bushing and installed handrail around rotary. Pulled diverter and L/D same." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled slipjoint. Installed master bushing." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Load shifted weight from tension system to BOP carrier. N/D tension system Disconnected BOP NT-2 connector" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Skidded BOP off well center." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed scaffolding" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing. Installed handrails around rotary." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lifted riser joint off WH, L/D same on drill floor. Installed hatch in moonpool. Installed master bushing" "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Cleaned and inspected TH area. Took pictures of locking ring." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Discussed plan forward with onshore organization. Performed SJA for remedial work on TH." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: R/U equipment to drill holes in activation ring and stop ring in TH. Mounted anchor ring and drilling machine onto WH." "On 2016-09-05, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Drilled hole in TH activation ring and stop ring. Slow progression to begin with, increased after first 4-5mm drilled." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 7.5 hours. Operational details: Continued drilling 4 ea holes. Worn out one bit each hole. Spent approximately 1,5 hour each hole. Experienced slow progress at the end of fourth hole due to wear on bit." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared TH profile." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D TH drilling equipment from WH." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Worked free stop ring and activation ring from TH. Observed dirt below stop ring, which possibly prevented activation ring to stroke up to fully released position. Removed stop ring and activation ring. TH lock ring collapsed out of locking grooves. Removed lock ring. Meanwhile: Performed TBT for N/U BOP" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed hatch. Pulled master bushing." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lowered HP riser joint from drill floor to WH. M/U connector on WH Installed hatch around riser." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed scaffolding around riser in moonpool." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Skidded BOP over well center. Landed onto riser joint. M/U BOP connector on riser joint." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed slipjoint. Installed masterbushing." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Installed tension cylinders to BOP. Meanwhile: Prepared diverter." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U bolts on slipjoint." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Insalled diverter." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Load shifted weight from BOP carrier to tension system. Pressurized diverter system, koomey unit and overshot." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Filled BOP with SW" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed BOP connector test to 20/235 bar for 5/10min. Meanwhile: R/U spooling unit for control lines." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: M/U BPV RT" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ BPV RT on 3 1/2' DP" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Retrieved BPV dart." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: RIH with BPV RT on 3 1/2' DP Retrieved BPV plug" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U handling equipment for 5 1/2' Meanwhile: Performed TBT for running spear BHA." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Reconfigured spear BHA in order to handle TH at surface. B/O and L/O double 5 1/2' DP." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2774m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH w/spear BHA to 25m. Engaged spear" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2774m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled tubing free, 10 ton OP." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2761m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH w/ tubng on spear. L/D 1 single 5 1/2' DP (due to space out on surface)." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2761m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U casing equipment" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2761m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U casing tong" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2748m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH w/ tubing and tubing hanger on spear." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2748m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: B/O and L/D down spear." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2748m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: B/O and L/D down tubing hanger" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2748m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installing slips" "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2744m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed BX-4 inserts to 7'. P/U tubing. Removed master bushing. Installed FMS slips." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2744m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH and removed clamp. L/O 2 ea 7' pup joints to cantilever." "On 2016-09-06, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2711m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH w/ 7' tubing from 2744 mMD to 2711 mMD. Avg pulling speed 4 jnt/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2557m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: POOH w/ 7' tubing from 2744 mMD to 2557 mMD. Avg pulling speed 6,5 jnts/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2463m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH w/ 7' tubing from 2557 mMD to 2463 mMD. Avg pulling speed 8 jnts/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2351m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH w/ 7' tubing from 2463 mMD to 2351 mMD. Avg pulling speed 10 jnts/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2276m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH w/ 7' tubing from 2351 mMD to 2265 mMD. Avg pulling speed 6 jnts/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2257m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH w/ 7' tubing from 2265 mMD to 2257 mMD. L/D DHSV assy" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2186m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH w/ 7' tubing from 2257 mMD to 2186 mMD. Avg pulling speed 11 jnts/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2186m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Counted joints on deck. Prepared to RIH with tubing on 5 1/2' DP" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2186m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: M/U swedge with pre-installed combination wiper." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2186m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/D casing equipment" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2186m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/D casing handling equipment. Removed control line spool." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2186m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Changed BX elevator inserts to 5 1/2' DP. Meanwhile: Cleaned and cleared drill floor." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2188m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U and M/U 5 1/2' stand, M/U to swedge. Changed to PS-21 slips and function tested same." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2460m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: RIH closed ended w/ tubing on 5 1/2' DP from 2188 m to 2460 m. Avg. tripping speed 530 m/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2460m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Filled pipe" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2770m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: RIH closed ended w/ tubing on 5 1/2' DP from 2460 m to 2770 m. Avg. tripping speed 530 m/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2770m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for displacement Observed losses on TT due to heavy fluid in annulus seeping past pre-installed wiper in tubing." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2770m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U and M/U pump-in sub. Installed lo-torque valve." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2770m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lined up to rig pumps. Initiated circulation, staged up pumps to 3000 lpm / 153 bar. Displaced well to SW." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2769m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U 1 m above combination wiper after 51 m3 of SW pumped. Continued displacing well to SW at 2200 lpm / 58 bar, until OIW content below 30ppm. Pumped totally 151 m3 of SW." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2769m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed cement hose Meanwhile: Performed TBT for cement job" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2769m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Balanced cement plug in 9 5/8' csg (2769 m - 2569 m ): Pumped 20 m3 wash pill, 2300 lpm/ 60 bar. Mixed and pumped 9,4 m3 of 1,90 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 2890 l of FW. Zeroed stroke counters. R/D cement hose. Displaced the cement with 39,6 m3 (1788 strokes) of SW, 3200 lpm/ 90 bar, using rig pumps." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2769m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: B/O and L/D pump-in sub." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ tubing restricted on 5 1/2' DP from 2769 m to 2570 m. 4 min/std." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: M/U pup with pre-installed sponge ball. Lined up to discharge returns. Pumped 10m3 hi-vis pill. Circulated 4,3 x B/U, 2300 lpm/ 55 bar." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: M/U BOP cleaning tool" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2570m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Cleaned BOP 10 x passes, 1500 lpm." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2540m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH 1 stand, L/D BOP cleaning tool" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2177m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: POOH w/ tubing on 5 1/2' DP from 2540 m to 2177 m. Avg. tripping speed 300 m/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2177m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed elevator inserts to 7'. Meanwhile: Performed TBT for R/U casing tong" "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2177m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U casing tong." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2177m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: B/O pup and swedge, L/D same." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2177m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed elevator inserts to 5 1/2' R/D casing tong." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2177m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U 7' spear BHA from HTS." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2508m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Engaged spear in 7' tubing at surface. RIH w/ tubing on 5 1/2' DP from 2177 m to 2508 m. Avg. tripping speed 440 m/hr." "On 2016-09-07, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2508m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: WOC Meanwhile: Serviced TDS. Removed casing tong for pulling 7' tubing. Installed casing tong for pulling 10 3/4' casing in fox hole." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2508m. The activity was categorized as 'interruption -- wait' and lasted for 6.5 hours. Operational details: WOC Meanwhile: - Continued working on TDS, aligned saver sub. - Changed hydraulic hose on TDS retract system - Inspected saver sub - Prepared and measured upcoming BHAs - Bled off B-annulus. 2 bar trapped, bled off all pressure - Performed PMs - Performed housekeeping at WH deck" "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2549m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U 1 5 1/2' DP stand and RIH w/ tubing from 2508 m to 2549 m. M/U TDS to DP." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2549m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for tagging TOC and leave tubing in well." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2620m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Initiated flow 550 lpm / 10 bar. Washed down slowly to 2620 mMD and attempted to tag TOC. Took weight gradually, 8 ton, indicating green cement." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2600m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH to 2600 mMD. Circulated 500 lpm / 10 bar." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2587m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH to 2587 mMD while circulating 500 lpm / 10 bar. Increased flow to 1500 lpm / 63 bar, circulated B/U while discharging cement contaminated returns." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2587m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: WOC while circulating at 500 lpm / 10 bar." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 2621m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Washed down slowly with 550 lpm / 10 bar. Observed pressure slighly increasing to 15 bar. Reduced flow rate to 200 lpm / 2 bar. Tagged TOC with 10 ton at 2621 mMD. Set down all tubing weight and disengaged spear." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 362m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: B/O TDS Dropped 3' drift." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ spear BHA on 5 1/2' DP from 362 m to 15 m. Avg. tripping speed 600 m/hr." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: L/D single 5 1/2' DP. R/B spear BHA." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: P/U and M/U jet sub." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 23m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: RIH w/ jet sub on 5 1/2' DP to 23 m." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 23m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cleaned MS-T seal assy surface with 1500 lpm / 22 bar. Made 3 x passes." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: POOH w/ jet sub on 5 1/2' DP from 23 m to surface." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: L/D Jet sub." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U MS-T seal retrieval tool." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U control lines to MS-T retrieval tool. Function tested retrieval tool." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH with MS-T retrieval tool to 20 m. Set down 2 ton. M/U TDS Engaged tool, managed to achieve 2,5 turns left. Ran hydraulic sequence to release MS-T seal." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled MS-T seal free with 70 ton OP." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with MS-T retrieval tool and seal assy to surface." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D control lines from MS-T retrieval tool. L/D retrieval tool." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 9m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U and M/U cutter BHA for cutting 10 3/4' surface tie-back." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 117m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from 9 m to 117 m." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 123m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Established parameters: 200 lpm / 7 bar, 400 lpm / 48 bar, 500 lpm / 81 bar, 600 lpm / 116 bar. 40 rpm / 2 to 4 kNm, 80 rpm / 2 to 5 kNm, 100 rpm / 2 to 6 kNm. Up/down weight 72/68 ton. Positioned cutter at 123 m and cut 10 3/4' tie-back casing, 100 rpm / 3 to 8 kNm, 400 lpm / 49 bar. Observed pressure drop, indicating casing cut." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 123m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Pulled up while circulating at 500 lpm, observed pressure increasing to 111 bar. Ran in slowly with rotation, observed pressure dropped to 3 bar when knifes entered cut." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: POOH w/ 10 3/4' cutter BHA on 5 1/2' DP from 123 m to surface." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D cutter BHA to HTS." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U spear BHA from set-back. Inspected grapple." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH w/ 10 3/4' spear BHA on 5 1/2' DP from surface to 25 m. Engaged spear and attempted to pull 10 3/4' surface tie-back casing, 30 ton OP." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.1 hours. Operational details: Disengaged spear and POOH to surface. R/B spear BHA." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: P/U 10 3/4' cutter BHA from HTS. Adjusted sweep and physical stop on cutters." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 123m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RIH w/ 10 3/4' BHA on 5 1/2' DP from surface to 123 m. M/U TDS" "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 123m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Initiated rotation and flow, 100 rpm / 2 to 6 kNm, 500 lpm / 81 bar. Cut 10 3/4' surface tie-back casing. Observed slight knock in riser and pressure dropped, indicating successful cut. Observed mud like substance on shaker, switched on gas trap. No gas observed." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 123m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flowchecked well for 10 min prior to POOH, static." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: B/O TDS. POOH w/ 10 3/4' cutter BHA on 5 1/2' DP from 123 m to surface." "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: L/D cutter BHA" "On 2016-09-08, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Reset and calibrated spinner wrench on IRN." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.1 hours. Operational details: P/U 10 3/4' spear BHA from set-back." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 25m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: RIH w/ 10 3/4' spear BHA on 5 1/2' DP from surface to 25 m. Engaged spear in tie-back casing." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH w/ spear and tie-back casing on 5 1/2' DP from 25 m surface." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed bushings in rotary. Released spear at surface and R/B same." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for pulling 10 3/4' surface tie-back." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: R/U casing tong. Changed to BX-3 elevator. Changed PDM head to handle 10 3/4'." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: POOH with 10 3/4' tie-back casing. Avg pulling speed 6,5 jnt/hr. Used manual slips and dog collar." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: L/D cut casing joint to HTS." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/D handling equipment." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for releasing tie-back adapter." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U torque tool BHA" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with 3 singles LH thread 5 1/2' DP" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Changed to LH thread saver sub" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued changing to LH thread saver sub, M/U to 95 kNm." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U and inspected torque tool. RIH w/ torque tool BHA on 5 1/2' LH thread DP to 139,8 m." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Latched dogs in tie-back adapter. Released tie-back connector by rotating left, 10 kNm." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH w/ torque tool BHA on 5 1/2' LH thread DP from 139,8 m surface. Set BHA in slips." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Changed from left threaded saver sub to normal saver sub." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D torque tool BHA" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U 10 3/4' spear BHA. Inspected tools." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 127m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH with 10 3/4' spear BHA on 5 1/2' DP to 127m. Engaged spear." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH w/ spear BHA and tie-back adatper on 5 1/2' DP from 127 m to surface." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for handling fish at surface" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O tie-back adapter and remaining casing. R/B spear BHA." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT for handling guns" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Changed BX elevator inserts and IRN dies. Installed barriers for handling explosives." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 17m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.5 hours. Operational details: P/U and M/U 10 3/4' perforation guns" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: RIH w/ 10 3/4' guns on 5 1/2' DP to 148 m." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: M/U TDS, confirmed line up and filled string. B/O TDS and dropped ball. M/U TDS. Spaced out to 147,5 m. Closed MPR and opened choke. Pressured up string to 140 bar with rig pumps, 150 lpm. Fired guns, pressure dropped to 5 bar, good indications." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Circulated 1000lpm / 11 bar, took returns through choke and poor boy. Observed max 1 ppm H2S in gas trap, no gas." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Flowchecked well for 5 min over choke, static. Flowchecked well for 10 min on TT, static." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 17m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: POOH w/ 10 3/4' guns on 5 1/2' DP from 147,5 m to 17 m." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: P/U and inspected guns, all shots fired. Meanwhile: Performed TBT for handling guns." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: L/D perforation guns." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 7m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U 10 3/4' cutter BHA. Inspected tools." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 319m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ 10 3/4' cutter BHA on 5 1/2' DP from 7 m to 319 m (bit depth) / 317 m (cutter depth)." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 319m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: M/U TDS and filled pipe. Recorded parameters: 200 lpm / 8 bar, 300 lpm / 21 bar, 400 lpm / 38 bar, 500 lpm / 72 bar, 600 lpm / 102 bar. Up/down weight 79/75 ton. 80 rpm / 2 to 6 kNm." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 319m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Attempted to cut 10 3/4' casing at 317 m, 500 lpm / 64 bar, 80 rpm / 4 to 11 kNm. Knock in string observed and torque decreased. No pressure drop observed. Pulled up 1 m above cut, no change in SPP observed. Ran in 0,5m below cut, no change in SPP observed and no tag of cut." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 318m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Re-cut 10 3/4' casing at 316 m, 500 lpm / 64 bar, 80 rpm / 4 to 11 kNm. Observed decreasing torque trend, no pressure drop observed. Cut until torque fell back to free rotational torque." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 318m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed 10 min flowcheck, static." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: POOH w/ 10 3/4' cutter BHA on 5 1/2' DP from 318 m to surface." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D cutter BHA on drill floor due to too much wind for crane operations." "On 2016-09-09, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Continued cleaning and clearing drill floor" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT for milling 10 3/4' casing hanger Meanwhile: Performed drops inspection on TDS" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 76m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: P/U and M/U 12 1/4' CH milling BHA." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: RIH w/ 12 1/4' CH milling BHA on 5 1/2' DP from 71 m to 138 m." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: M/U TDS and filled pipe. Recorded parameters; up/down weight 82/78 ton, 80 rpm / 2-6 KNM, 2000 lpm / 11 bar." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 143m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Tagged 10 3/4' CH with CH mill at 141,26 m w/ 4 ton. Marked pipe." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 143m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.5 hours. Operational details: Milled 10 3/4' casing hanger from 141,26m to 141,55m, 1500-2000 lpm / 12-15 bar, 80-100 rpm / 9-12 kNm, WOB 1-6 ton. Got good indications that casing parted from CH. Torque decreased to 2 to 6 kNm after milling 29cm, observed small gas peak of 1% and 1 ppm H2S in gas trap. Pulled up 1 m with flow and rotation, no restrictions. Stopped rotation and slided down through CH area, no restriction." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 144m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Continued sliding down and tagged top of 10 3/4' casing at 142,66 m. Dressed off 10 cm of top of casing, 2000 lpm / 15 bar, 80-100 rpm / 7-9 kNm, WOB 3-8 ton." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Pulled up and placed taper mill above CH. Circulated 2 x B/U, 3000 lpm / 20 bar." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Flowchecked well for 10 min, static. Meanwhile: Performed TBT for drops inspection." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Performed drops inspection on TDS, moonpool, derrick and drill floor. No findings." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 142m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed TBT for manual handling" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 108m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: POOH w/ 10 3/4' CH milling BHA on 5 1/2' DP from 142 m to 108 m." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 108m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor. L/O cutter BHA, which was previously left on drill floor due to wind restriction on crane." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 70m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Continued POOH w/ 10 3/4' milling BHA on 5 1/2' DP from 108 m to 70 m. Over-torqued connections due to vibrations during milling." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Continued POOH w/ 10 3/4' milling BHA on 5 1/2' DP from 70 m to surface." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Cleaned string magnet, 22kg swarf. L/D 10 3/4' milling BHA." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TOFS. Cleaned and cleared walkways and escape routes on drill floor. Meanwhile: Function tested BSR." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: P/U 10 3/4' spear BHA. Inspected and serviced grapple. Set spear in catch mode." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: RIH w/ 10 3/4' spear on 5 1/2' DP from surface to 148 m. Pulled up and verified spear engaged in 10 3/4' casing, 88 ton on weight indicator." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 205m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: POOH with 10 3/4' casing on 5 1/2' DP from 316 m to 205 m." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 205m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Flowchecked well for 10 min, static. Meanwhile: Performed TBT for releasing spear at surface." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 191m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: POOH to 191 m and L/D 1 single 5 1/2' DP." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 191m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: R/U handling equipment for 10 3/4' casing" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 175m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: POOH to 175m. Set slips on casing. Disengaged spear. R/B spear BHA." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 175m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: B/O 10 3/4' casing pup and L/O same." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 175m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Changed to casing elevator dressed for 10 3/4'." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.5 hours. Operational details: POOH with 10 3/4' casing from 175 m surface. Average pulling speed 6,2 joints/hr. Used manual slips and dog collar. L/O cut casing joint." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/D handling equipment for 10 3/4' casing. Changed to elevator for 5 1/2' DP handling." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for running 13 3/8' EZSV plug" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: P/U and M/U 13 3/8' EZSV RT and plug. Installed springs on tool." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 303m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: RIH w/ 13 3/8' EZSV plug on 5 1/2' DP from surface to 303 m. Avg. tripping speed 450 m/hr." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 303m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Recorded up/down weight, 77/73 ton. Established circulation and washed the setting area, 800lpm/ 4 bar. Installed the 13 3/8' EZSV plug at 303 m. Load tested the plug with 10 ton." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Pumped 10m3 wash pill and 10 m3 push pill followed by SW while rotating string 50 rpm. Circulated until clean SW in returns, 2500 lpm / 16 bar." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for cement job" "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: B/O double 5 1/2' DP. M/U pump-in sub to string. M/U TDS. Spaced out 3m above EZSV plug." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed cement hose. Leak tested cement line to 100 bar for 2 min." "On 2016-09-10, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 10m3 drill water with rig pumps, 2500 lpm / 14 bar. Mixed and pumped 7,8 m3 1,93 sg cement slurry, 600 lpm / 16 bar. Displaced cement with 2 m3 drill water, 600lpm / 14 bar, using cement unit." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: B/O and L/O pump-in sub. M/U double 5 1/2' DP to drill string." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 180m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH restricted w/ EZSV RT on 5 1/2' DP from 300 m to 180 m. 2min/std." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 180m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed pup with pre-loaded sponge ball. M/U TDS. Circulated 2 x B/U, 2500 lpm/ 13 bar at 50 rpm. Discharged cement contaminated returns." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 180 m to 115 m." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U and M/U BOP wash tool and FOSV." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Washed BOP by pumping SW at 1600 lpm, 80 rpm, 3 x passes." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Functioned BOP rams and washed additional 3 passes" "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Flowchecked well for 10min, static. Meanwhile: B/O and L/D BOP washing tool." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 120 m to surface." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: L/D EZSV RT." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Drained riser through B-annulus outlet on WH. Meanwhile: Installed chains on TDS for pulling diverter. R/U fence around rotary." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling diverter" "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Attempted to pull diverter. Adjusted tension cylinders while holding 3-4 ton overpull." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew for pulling diverter." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled diverter and R/B same." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: N/D slipjoint and R/B same. Meanwhile: Performed pre-skidding checks." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Load shifted weight from tension cylinders to BOP carrier. N/D tension cylinders Meanwhile: Continued with pre-skidding checks." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Diconnected BOP connector. Lifted and skidded BOP off well center." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed scaffolding around HP riser." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U equipment to lift HP riser." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Disconnected NT2 connector on WH. Removed WH hole covers. Pulled HP riser from WH to drill floor. L/D riser." "On 2016-09-11, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed scaffolding in moonpool. Meanwhile: Performed TBT for moving hatches in moonpool. ******** END OF REPORT ********" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding rig" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded rig AFT to well F-5" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Built handrail scaffold in moonpool. Meanwhile: Performed post-skid checks." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Removed hatch in moonpool" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Built ring/fence around deck openings. Meanwhile: Performed TBT to run NT2 connector." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled master bushing and removed fence around rotary. Ran NT2 connector and installed same on multibowl." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U and M/U cutter BHA" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U Multibowl RT to inner string. Recorder up/down weight 75/72 ton. RIH and engaged Multibowl RT to multibowl by rotating elevator. M/U TDS." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for removal of tension cylinders" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.2 hours. Operational details: Bled off pressure on tension cylinders and transfered load to TDS. R/D tension cylinders, hubs and tensioner ring. Removed boat collision stool and centralizers at all decks. Installed hoses to multibowl outlets. Meanwhile: L/O 21 joints 5 1/2' DP from set-back. Performed TBT for cutting riser." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Took tension, 20 ton overpull. Staged up flow rate to 2400 lpm / 90 bar. Cut riser, lost overpull, good indication of cut." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed hoses and outlets from Multibowl." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled riser until Multibowl at drill floor. Installed big C-plate and landed off riser." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: B/O Multibowl RT. Installed false rotary." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Parked AFT PRS w/ Multibowl RT in safe position." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled and R/B innser string." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/B cutting BHA" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U Multibowl RT" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled tensioner joint (Lift #1), cleaned riser for marine growth at centralizer deck. Installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Cut tensioner joint Significant wave height 2,7 m." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting machine" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O tensioner joint" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed running tool. Installed cradle on HTS frame. Removed elevator. Cleared drill floor." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for cut and pull riser joints" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lifted riser and removed master bushing." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled riser (lift #2). Cleaned off marine growth on centralizer deck (relatively big amounts of growth on spash zone joint)." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled riser flange to drill floor. Installed master bushing and elevator. Removed fairing and landed riser onto elevator." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine" "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Cut riser joint. Knifes jammed several times possibly due to movement. Changed 1 knife due to wear. Significant wave height between 2,8 and 3,3 m." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting machine." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (lift #2)." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (lift #3) Installed elevator and master bushing. Landed riser onto elevator." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine. Cut riser. R/D cutting machine. Significant wave height 3,5 m." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (lift #3)." "On 2016-10-13, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled riser out of splash zone (lift #4)." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled riser flange above rotary (lift #4). Installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine. Cut riser." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting machine." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (lift #5). Installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U cutting machine. Cut riser. R/D cutting machine." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint" "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled riser (lift #6). Pulled flange through rotary, installed master and elevator. Landed riser onto elevator." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. R/D cutting machine." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint. Unable to move riser joint from HTS to cantilever due to wind above 40knts." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled master bushing. Pulled riser through rotary (lift #7). Installer master bushing and hole cover." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint #6 and #7 to cantilever." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed elevator." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/D tension cylinders left hanging in the top mounting point." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.8 hours. Operational details: Waited on weather for pulling production risers Meanwhile: R/D tension cylinders. Reconfigured cutter BHA and R/B in different finger (blocked 5 1/2' DP to be L/O)." "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: Waited on weather for pulling production risers Meanwhile: Continued R/D tension cylinders. Stuck pin, needed to work loose. L/O 6 joints #24,7 and 35 joints #21,9 5 1/2' DP L/O 4 singles 5 1/2' HWDP Cleaned pits" "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on weather for pulling production risers Meanwhile: Performed skidding checks. Performed DROPS inspection in derrick, STB crane pedestal, production main deck and cantilever walkways. Continued R/D tension cylinders. Lifted 3 x tension cylinders and boat collision stool from WH to drill floor. Cleaned pits Cleaned shakers" "On 2016-10-14, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather for pulling production risers Meanwhile: Continued R/D cylinders on well F-4 and F-5. Cleaned pits and shakers" "On 2016-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: Waited on weather for pulling production risers Meanwhile: Lifted equipment from well F-4 and F-5 from WH deck to drill floor (cylinders, centralizers, boat collision stool etc.) Cleaned pits and shakers" "On 2016-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on weather for skidding cantilever and pulling production risers Too strong wind to skid. Meanwhile: Installed moonpool hatch. Removed scaffolding and handrail on WH deck. Cleaned pits and shakers" "On 2016-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: Waited on weather for skidding cantilever and pulling production risers. Too strong wind to skid Meanwhile: Cleaned trip tanks Assisted removal of pit sensors Cleaned shakers Opened BOP and inspected cavities Opened annular preventer and inspected same" "On 2016-10-15, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather for skidding cantilever and pulling production risers. Too strong wind to skid Meanwihle: Continued cleaning shakers Continued inspecting BOP and ram cavities Open and inspected dry bulk silos" "On 2016-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: Waited on weather for skidding cantilever and pulling production risers. Too strong wind to skid. Meanwhile: Continued cleaning shakers Continued inspecting BOP Continued inspecting dry bulk silos" "On 2016-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather for skidding cantilever and pulling production risers. Too strong wind to skid Meanwhile: Performed TBT for skidding" "On 2016-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.8 hours. Operational details: Waited on weather for skidding cantilever and pulling production risers. Too strong wind to skid Meanwhile: Continued cleaning shakers Continued inspecting BOP Continued inspecting dry bulk silos" "On 2016-10-16, at Well NO 15/9-F-5, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.8 hours. Operational details: Waited on weather for skidding cantilever and pulling production risers. Too strong wind to skid Meanwhile: Cleaned shaker pits and upper shakers. Continued inspection of dry bulk silos. Assembled annular preventer Inspected BOP ram cavities **** END OF REPORT ****" "On 2008-12-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1467m. The activity was categorized as 'drilling -- drill' and lasted for 9.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 1381 m to 1467 m MD. Invalid surveys due to interference from adjacent 9 5/8' casing. Drilling parameters : 4000-4500 lpm / SPP 188-230 bar / 1-4 MT WOB / 80-100 RPM / Torque 6-10 kNm / ECD 1,43-1,47. Controlled ROP to 12 m/hrs as dictated by cuttings handling. Downlinked powerdrive as per DD instructions." "On 2008-12-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1478m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 1467 m to 1478 m MD. Obtained first good survey at 1478 m MD. Drilling parameters : 4500 lpm / SPP 228 bar / 3 MT WOB / 80-100 RPM / Torque 10 kNm / ECD 1,43-1,44. Attempted to increase ROP to 20 m/hrs, resulted in blockaged in cuttings injection system (active tank). Dercreased ROP to 15 m/hrs as dictated by cuttings handling. Downlinked powerdrive according to DD instructions." "On 2008-12-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1525m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 1478 m to 1525 m MD. Drilling parameters : 4500 lpm / SPP 227 bar / 2-3 MT WOB / 130 RPM / Torque 9-12 kNm / ECD 1,43-1,44. Controlled ROP to 18 m/hrs as dictated by cuttings handling. Downlinked powerdrive according to DD instructions." "On 2008-12-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1608m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled and oriented 17 1/2' hole from 1525 m to 1608 m MD. Drilling paramaters : 4500 lpm / SPP 236 bar / 3-4 MT WOB / 130 RPM / torque 10 kNm / ECD 1,44-1,45 Controlled ROP to 18 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions." "On 2008-12-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1635m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and oriented 17 1/2' hole from 1608 m to 1635 m MD. Got problems with cuttings handling. Mill loop on active tank got blocked. Worked to unblock line. Meanwhile continued drilling at lower ROP and routed cuttings to skips as required. Drilling parameters : 4000 lpm / SPP 195 bar / 2-3 MT WOB / 130 RPM / torque 8-10 kNm / ECD 1,44. Controlled ROP to 5-10 m/hrs as dictated by cuttings handling and toubleshoting." "On 2008-12-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1761m. The activity was categorized as 'drilling -- drill' and lasted for 9.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 1635 m to 1761 m MD. Drilling paramaters : 4500 lpm / SPP 237-244 bar / 4-6 MT WOB / 130 RPM / Torque 7-13 kNm / ECD 1,44-1,45. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions." "On 2008-12-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1801m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and oriented 17 1/2' hole from 1761 m to 1801 m MD. Drilling paramaters : 4500 lpm / SPP 245 bar / 6-8 MT WOB / 130 RPM / torque 10-13 kNm / ECD 1,43-1,44. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions. Had problems with spooling on PRS lift wire drums." "On 2008-12-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1801m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed flush joint elevator on PRS in order to fix spooling problem. Ran gripper head to floor and re-spooled drums. Meanwhile reamed on stand and downlinked powerdrive." "On 2008-12-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1833m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 1801 m to 1833 m MD. Drilling paramaters : 4500 lpm / SPP 246 bar / 5-7 MT WOB / 130 RPM / torque 12 kNm / ECD 1,43-1,44. Controlled ROP to 20 m/hrs due to cuttings handling." "On 2008-12-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1841m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled and oriented 17 1/2' hole from 1833 m to 1841 m MD. Drilling parameters : 4500 lpm / SPP 248 bar / 6 MT WOB / 140 RPM / torque 8-12 kNm / ECD 1,44. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions." "On 2008-12-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1841m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.8 hours. Operational details: Waited on weather. Winds > 65 knots, i.e. in excess for PRS operational limit. Meanwhile performed MWD surevy and downlinked powerdrive. Reciprocated on stand from 1841 m to 1801 m MD. Parameters : 3000 lpm / SPP 120 bar / 50 RPM / torque 9 kNm / ECD 1,43-1,44." "On 2008-12-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2047m. The activity was categorized as 'drilling -- drill' and lasted for 12.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 1841 m to 2047 m MD. Drilling parameters : 4500 lpm / SPP 252-258 bar / 2-6 MT WOB / 140 RPM / torque 11-14 kNm / ECD 1,44-1,46. Controlled ROP to 20-22 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions." "On 2008-12-14, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2084m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 2047 m MD to 2084 m MD. Drilling parameters : 4500 lpm / SPP 261 bar / 2-3 MT WOB / 140 RPM / Torque 9-13 kNm / ECD 1,45. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions. Experienced problems when picking up 5 1/2' stand. Meanwhile made up 13 3/8' casing stands in foxhole." "On 2008-12-14, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2084m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: When attempting to pick up a stand of 5 1/2' DP, the stand was bent. Probable cause is that the stand was caught by the wind and/or hit by the flush joint elevator when making the grip with the gripper head. Hence the stand was bent when retracting the arm. Closed additional fingers to secure the stand in the finger slot. Set down stand and made new grip. Inspected stand visually, stand seemed to by straight and undamaged. Meanwhile reciprocated stand with 3000 lpm / 80 RPM." "On 2008-12-14, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2134m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and oriented 17 1/2' hole from 2084 m MD to 2134 m MD. Drilling parameters : 4500 lpm / SPP 264 bar / 3-7 MT WOB / 140 RPM / torque 11-16 kNm / ECD 1,45. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions. Meanwhile made up 13 3/8' casing stands in foxhole." "On 2008-12-14, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2310m. The activity was categorized as 'drilling -- drill' and lasted for 11.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2134 m to 2310 m MD. Drilling parameters : 4500 lpm / SPP 267-274 bar / 3-8 MT WOB / 120-140 RPM / torque 13-22 kNm / ECD 1,45-1,46. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions." "On 2008-12-14, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2318m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled and oriented 17 1/2' hole from 2310 m to 2318 m MD. Reduced ROP to 10 m/hrs due to plugged line in DCI system. Routed cuttings to skips while working to unplug line. Drilling parameters : 4000-4500 lpm / SPP 221-268 bar / 4-5 MT WOB / 120 RPM / torque 16 kNm / ECD 1,45." "On 2008-12-14, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2401m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2318 m to 2401 m MD. Drilling parameters : 4500 lpm / SPP 275 bar / 5-7 MT WOB / 125 RPM / torque 16-20 kNm / ECD 1,45-1,46. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions." "On 2008-12-15, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2447m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2401 m to 2447 m MD. Drilling parameters : 4000-4500 lpm / SPP 222-276 bar / 7-9 MT WOB / 125-140 RPM / torque 18-22 kNm / ECD 1,45-1,46. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions. Prepared manriding operation for inspecting and repairing hydraulic leak on PRS." "On 2008-12-15, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2447m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed manriding to hose bundle in top of PRS. Thightened fittings on several hoses. Inspected and found leak to be fixed. Meanwhile circulated at 3000 lpm / SPP 136 bar." "On 2008-12-15, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2474m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2447 m to 2474 m MD. Drilling parameters : 4500 lpm / SPP 274 bar / 8-9 MT WOB / 140 RPM / torque 20-22 kNm / ECD 1,45. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions. Meanwhile made up 13 3/8' casing in stands using PRS and foxhole." "On 2008-12-15, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- drill' and lasted for 10.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2474 m to section TD at 2591 m MD. Drilling parameters : 4500 lpm / SPP 274 bar / 8-10 MT WOB / 140 RPM / torque 20-32 kNm / ECD 1,45. Controlled ROP to 20 m/hrs due to cuttings handling. Performed MWD survey on connections. Downlinked powerdrive according to DD instructions. Meanwhile made up 13 3/8' casing in stands using PRS and foxhole." "On 2008-12-15, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated hole clean while reciprocating last stand from 2591 m to 2569 m MD. Parameters : 4200-4500 lpm / SPP 246-272 bar / 140 RPM / torque 13 kNm / ECD 1,43-1,44." "On 2008-12-15, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2565m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: Set back stand of DP and continued circulating hole clean while reciprocating stand from 2565 m to 2526 m MD. Parameters : 4200-4500 lpm / SPP 246-274 bar / 85 RPM / torque 13 kNm / ECD 1,43-1,44. Circulated a total of 4 x bottoms up until clean shakers." "On 2008-12-15, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2565m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Lined up to triptank and flowcheked well. Observed static losses to well in order of 350 l/hrs. Checked trip tank line up - ok." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2565m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Discussed situation. Decided to attempt sweeping hole and place LCM pill across the Grid formation. Mixed and weighed 1,43 sg / 167 kg/m3 Calcarb/Steelseal LCM pill. Meanwhile circulated in well at 4500 lpm / SPP 277 bar." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2568m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Pumped 19 m3 LCM pill and chased same with 64 m3 of OBM to put pill accross the Grid formation. Pumprate 2000 lpm / SPP 68 bar / 30 RPM." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2568m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Lined up triptank and flowchecked well - prevailing loss trend - still loosing approx 350 l/hrs. Discussed situation, decided to start POOH." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2366m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 2568 m to 2366 m MD. Pulled 5 stands wet." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1764m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Pumped 4 m3 1,63 sg slug allowed mud level to stabilize. POOH with 17 1/2' drilling BHA on 5 1/2' DP from 2366 m 1764 m MD." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1764m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well 15 min due to apparently decreasing loss trend. Well static." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1385m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Filled triptanks. POOH with 17 1/2' drilling BHA on 5 1/2' DP from 1764 m to 1385 m MD. Took 10-15 MT overpull av 1385 m MD." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Made up TDS to drillstring in order to work through restriction from 1385 m MD. Broke circulation and staged up pumps to 3000 lpm / SPP 111 bar. Rotated at 15-50 rpm and worked area from 1385 m to 1357 m MD. Observed torque peaks of 20 kNm at 1370 and 1381 m MD. Stopped rotation and circulation and pulled from 1385 m to 1357 m MD with no overpull. No overpull detected at shoedepth 1368 m MD." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Flow checked well at casing shoe. Observed static losses of 130 /l/hrs. Removed skirt on TDS torque wrench and took measurements for Tesco equipment as required." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pumped 5 m3 1,67 sg slug." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 1357 m to 147 m MD. Tripping speed 806 m/hrs." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flowchecked prior to POOH with BHA - well static. Meanwhile re-arranged equipment on drillfloor for racking 17 1/2' drilling BHA due to winds exceeding set limits for crane. Held toobox talk for racking back BHA." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Removed PS-30 slips from rotary. Installed masterbushing and bowl. Re-arranged equipment on drillfoor as required for racking BHA." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 17 1/2' dirlling BHA. Broke and racked back 5 1/2' HWDP, DC/accellerator, DC/jar, NMDC/DC and ARC/powerpulse/powerdrive. Gauged and graded bit." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Cleaned and tidied drillfloor." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up jet sub. Picked up and made up WBRRT. RIH on 5 1/2' DP from surface to 140 m MD. Jetted BOP on way in at 3400 lpm / SPP 22 bar." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Jettted across wellhead at 1800 lpm / SPP 18 bar. Pulled nominal seat protector in wellhead." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with WBRRT on 5 1/2' DP from 140 m MD to surface. Released NSP from WBRRT. Broke and laid out WBRRT and jet sub." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared and tidied drillfloor. Inspected aft PRS rollers and dies prior to casing running." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging casing running equipment." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Changed elevator on TDS. Installed FJE in aft PRS." "On 2008-12-16, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Installed casing tong on IR tracks. Made up DP x-over to 13 3/8' casing swadge. Meanwhile lined up cement unit to pump down F-14 injection annulus. Stepped up pressure from 126 bar to 138 bar when sudden leak off to 60 bar was observed. Continued injection and stepped up pump rate to 1000 lpm / CUP 71 bar. Injected 150 m3 seawater at 1000-1200 lpm. After shut in the pressure stabilized at 50 bar after 1 hour (still 50 bar at 07:00)." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Hooked up and fuctioned casing tong. Removed masterbushing. Installed FMS in rotary -adapeter ring on FMS did not fit in rotary. Removed adapter ring and installed FMS in rotary. Changed fittings on hydraulic hoses and hooked up FMS to rig hydraulics. Attemped to function FMS - negative." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Not able to function FMS. Troubleshot situation. Changed fittings on hoses - still not functioning correctly. Traced external panel for FMS and hooked up same. Traced 13 3/8' inserts for PS-30. Hooked up FMS to external panel, functioned FMS - ok. Installed by-pass baffle in shoe joint laying on HTS." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for running casing." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up shoe joint. Attempted to run shoe joint, could not pass guides on FMS. Removed guides on FMS. Not able to run bow spring centralizer through FMS. Removed FMS and installed masterbushing and bowl." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 39m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with shoe joint, checked float for pos/neg flowthrough - ok, hung off on manual slips. Picked up and made up intermediate joint. Picked up and made up float collar joint. Threadlocked connections. Used dog collar to secure in slips. Filled joints with 1,43 sg OBM." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Ran 13 3/8' - P110 - 72# casing from 40 m to 140 m MD. Used manual slips. Filled every joint with 1,43 sg OBM." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for removing bushings." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed masterbushing and installed PS-30 slips. Had problems with hydraulics on PS-30." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot hydraulics on PS-30." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 184m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran 13 3/8' - P110 - 72# casing from 140 m to 184 m MD. Filled every 5th joint with 1,43 sg OBM." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 184m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk / handover meeting with new crew." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 783m. The activity was categorized as 'drilling -- casing' and lasted for 6.8 hours. Operational details: Ran 13 3/8' - P110 - 72# casing from 184 m to 783 m MD. Filled every 5th joint with 1,43 sg OBM. Running speed 7-8 jnts/hr." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 783m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Filled string and lined up to triptank - well static. Moved rollers on HTS to pick from aft bays." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 808m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Ran 13 3/8' - P110 - 72# casing from 783 m to 808 m MD." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 808m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk / handover meeting with new crew." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 914m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Ran 13 3/8' - P110 - 72# casing from 808 m to 914 m MD. Had problems with HTS rollers." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 914m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot problems with HTS rollers." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1035m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Ran 13 3/8' - P110 - 72# casing from 914 m to 1035 m MD. Filled every 5th joint with 1,43 sg OBM. Running speed 7 jnts/hr." "On 2008-12-17, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1035m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Halted operations due to incident on pipedeck. A wooden beam came flying over the HTS and landed accross the gangway on the oposite side of the HTS (i.e. starboard side). Took time out for investigation and debrief / safety brief." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1035m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Took time out for safety brief. Shot pictures to document incident." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Ran 13 3/8' - P110 - 72# casing from 1035 m to 1359 m MD. Filled every 5th joint with 1,43 sg OBM. Running speed 7-8 jnts/hr." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging Tesco casing running equipment. Lined up well to triptank -well static." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Removed elevator. Brought Tesco frame to well center. Not able to stab criculating packer into 13 3/8' casing. Rigged up DP elevator to apply more force on packer - still not able to enter 13 3/8' circulation packer in 13 3/8' casing. Secured frame for making up TDS." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Secured Tesco tool with slings and tuggers. Conneceted TDS to Tesco tool. Sat down weight to enter circulation packer into 13 3/8' casing." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Made up Tesco tool with torque wrench. Hooked up hydraulic and pneumatic controls on Tesco tool. Function tested tool, ok." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke circulation at shoe and stepped up pumps to 1500 lpm / SPP 11,5 bar. Pumped 38 m3 whilst moving rollers on HTS." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1371m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran 13 3/8' P110 72# casing from 1359 m to 1371 m MD. Not able to align/stab casing joint correctly when picking up with PRS pick up tool (FJE)." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1371m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Not able to stab to stab casing correctly. Crossed threads, negative make up. Backed out joint. Cleaned, inspected and refurbished threads." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1467m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Ran 13 3/8' P110 72# casing from 1371 m to 1467 m MD. Running speed 2 jnts/hr, restricted by alignment/stabbing problems when using PRS pick up tool." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1467m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Encountered tight spot at 1467 m MD. Broke circulation. Set down 25 MT. Applied 3 rpm within 15 kNm limit. Passed restriction." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1476m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Reciprocated string between 1469 m and 1476 m MD." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran 13 3/8¿ P110 72# casing from 1476 m to 1500 m MD. Encountered tight spot at 1481 m MD. Stepped up pumps to 900 lpm. Appled 3 rpm within 15 kNm limit. Worked restriction every 12 m indicating centralizers hanging up in shoe or kick off area. Max set down weight 25 MT. Set casing joint in foxhole prior to making 2nd grip with PRS pick up tool - this method seemed to make the stabbing more accurate." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1532m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Ran 13 3/8' P110 72# casing from 1500 m to 1532 m MD. Worked restriction every 12 m within set limits." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1532m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Encountered tight spot at 1532 m MD. Not able to pass with 25 MT setdown weight. Worked string several times in attempt to pass restriction. Pumped at 1000 lpm / 10 bar and rotated 5 RPM within 15 kNm limit. Increased set down weight to 30 MT and passed restriction. Observed pack off / rapid pressure build up to 20 bar - shut down pumps." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1532m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Staged up pumps in increments to 1500 lpm. Observed SPP dropping after a period of pumping at each stage. 500 lpm stabilized pressure of 12 bar. 1500 lpm stabilized pressure of 18 bar. Circulated bottoms up - no significant returns on shakers." "On 2008-12-18, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1556m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Ran 13 3/8' P110 72# casing from 1532 m to 1556 m MD. Filled casing string on every 5th joint run. No excessive drag in hole." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1912m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Ran 13 3/8' P110 72# casing from 1556 m to 1912 m MD. Filled casing string on every 5th joint run. No excessive drag in hole, but observed tight spot at 1719 m MD." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2441m. The activity was categorized as 'drilling -- casing' and lasted for 9.2 hours. Operational details: Ran 13 3/8' P110 72# casing from 1912 m to 2441 m MD. Filled casing string on every 5th joint run. No excessive drag in hole. Worked through tight spots at 2092 m and 2160 mMD with max circulation of 1300 lpm / 10-16 bar and max 30 MT weight added." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2441m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RD and LO Tesco tool." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2441m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Installed BX elevator and tilt adaptor." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2441m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: PU casing hanger and PADPRT assy. Reciprocated string while RD csg tong. Changed head on PDM and cleared rig floor. Changed PS 30 to master- and inner bushings. Observed 30 MT drag running casing hanger assy through rotary." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2478m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH to land 13 3/8' csg on 5 1/2' HWDP from 2441 m to 2478 m. Established circulation rate and washed down with 440 lpm/3.6 bar. Up weight 283 MT/ down weight 217 MT." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2478m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Reinstalled pipe handler skirt on TDS due to high winds making it difficult to stab into 5 1/2' HWDP stnd. Meanwhile continued circulating at 675 lpm / 5.0 bar." "On 2008-12-19, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2572m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Washed down to land 13 3/8' csg on 5 1/2' HWDP from 2478 m to 2572 m with 675 lpm/5.0 bar. Worked through tight spot at 2569 m MD with max circulation of 1100 lpm / 15 bar and max 20 MT weight added." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2577m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Worked 13 3/8' csg down from 2572 m to 2577 m MD with circulation of 1500-2300 lpm / 28-35 bar and max 30 MT weight added at approx 1 m/hr. Observed a significant amount of cuttings in return. Up weight 295 MT/ down weight 223 MT." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2579m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Worked 13 3/8' csg down from 2577 m to 2579 m MD with circulation of 2300 lpm / 30 bar and max 30 MT weight. Decreasing progress towards 2579 m. Observed rapid pressure increase when taking weight until 2579 m, where no pressure increase was seen. Unable to pass 2579 m with max 40 MT. Up weight 295 MT/ down weight 223 MT." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2538m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH with 13 3/8' P110 72# casing from 2579 m to 2538 m MD on 5 1/2' HWDP while circulating at 400 lpm / 5 bar. Observed rapid pressure increase to 35 bar and shut off pump at 2538 m. Meanwhile changed head on PDM." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2538m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: Attempted to free 13 3/8' csg by working string down, but pressure did not bleed off. Worked string with 35 MT upwards and 45 MT downwards. Pressure dropped off while working pipe upwards. Pumped 100 lpm while working pipe upwards (pressure increase when stopped pumping) and regained circulation at 2504 m. Staged up pumps to 2300 lpm / 27 bar." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2417m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Continued POOH with 13 3/8' P110 72# casing from 2538 m to 2449 m MD on 5 1/2' HWDP while circulating at 2300 lpm / 28 bar. Pulled master bushings. Installed csg tong. RB casing hanger assembly. Changed to BX-elevator." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2449m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH and LD 13 3/8' csg joint #69 and #70." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2426m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Changed to 5 1/2' elevator. PU and MU csg hanger assy. RIH with csg hanger below rotary 2417 m to 2426 m. Staged up pumps to 2300 lpm / 20 bar and established circulation whilst removing csg tong." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2557m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 13 3/8' P110 72# casing from 2426 m to 2557 m MD on 5 1/2' HWDP while circulating at 2300 lpm / 28 bar. Up weight 290 MT/ down weight 222 MT." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2557m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PU and MU cmt head." "On 2008-12-20, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2558m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Attempted to RIH and land 13 3/8' csg. Had 25 MT drag at 2558 m." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2558m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Staged up pumps to 1000 lpm / 9 bar and established circulation. Attempted to RIH and land 13 3/8' csg. Had 25 MT drag at 2558 m. Staged up pumps to 2000 lpm / 29 bar and worked pipe to pass tight spot at 2558 m. POOH 5-12 m 4 times and past tight spot." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Reduced flow rate to 500 lpm / 7 bar. Landed csg hanger according to Vetco procedure at 2562.4 m and sat down 7 MT off landing string weight. Rotated DP 1/4' turn to the right to ensure stem was free." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Staged up pumps to 3000 lpm / 57 bar and established circulation with 1.43 sg OBM. Circulated btms up (11750 strks) using rig pumps while performing pre-job safety meeting with involved personnel. Prepared tuned spacer." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Performed line test of cmt hose to 345 bar/10 min. Ok. Pumped 8 m3 of base oil at 1760 lpm followed by 20 m3 1.67 sg tuned spacer E at 1760 lpm using rig pumps. Chased spacer to drill floor with 3 m3 OBM. Lined up to pump from cmt unit. Opened lo-torque valve with 20 bar on cmt line to verify line-up. Released btm dart for btm plug. Mixed and pumped 23.25 m3 1.90 sg silica cmt slurry at 800 lpm / 32 bar and 7.0 m3 g-cmt slurry at 800 lpm/ 20 bar." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Displaced cmt to rig floor with 500 ltrs of DW at 1000 lpm. Released top dart and pumped 1500 ltrs at 1500 lpm behind cmt using cmt unit. Top wiper plug sheared at 158 bar after 750 ltrs pumped. Lined up through to top drive and zeroed stroke counters on mud pumps. Continued dispacing cmt by pumping OBM at 3000 lpm. Sheared btm plug at 7219 strks (159.8 m3) / 155 bar. Reduced rate to 1200 lpm at 8400 strks (185.7 m3). FCP was 53 bar. Bumped top plug at 8552 stks (189.0 m3) / 142 bar." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2562m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Pressured up surface lines to 140 bar to equalize and open lo-torque on cmt head. Attempted to close IBOP. No go. Bled off pressure to 95 bar, closed IBOP and continued to pressure up csg to 345 bar. Bled off standpipe pressure to 25.7 bar and monitored for leak through IBOP. Performed pressure test of 13 3/8' csg to 345 bar / 15 min, Ok. Bled back pressure to 20 bar and monitored for back flow. No back flow observed. 2.9 m3 pumped and 2.9 m3 bled back." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Sat seal assembly according to vetco procedure. Landing string dropped 8 1/4'. Performed line test of surface line against fail safe valve to 345 bar / 10 min. Ok. Closed lower pipe ram and lined up TDS to trip tank to monitor for returns. Pressured up in stages to 207 bar below closed ram. Bled off pressure to zero. Pumped 350 ltrs and got 300 ltrs back. Opened rams and took 45 MT overpull. Closed ram and pressure tested seal assembly 35/345 bar for 5/10 min. Dropped 3.5 bar (1 %) / 15 min. 550 ltrs pumped and 450 ltrs bled back. Reduced overpull to 3 MT. Rotated 4 right-hand turns and released." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: LD cmt head std. Dropped sponge balls and flushed string with 4400 lpm using OBM." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with PADPRT from 135 m to OOH. Removed PS21 and installed master bushings. Measured lead impression block to be 1.7'. LO PADPRT." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: MU and RIH with wear busing and WBRT. Washed well head and installed wearbusing at 139.3 m. POOH with WBRT and LO jet sub and WBRT." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 175m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: MU jet sub to HWDP and RIH from surface to 40 m. PU and MU 18 3/4' BOP test plug. RIH with BOP test plug on 5 1/2' DP from 40 m to 175 m and landed off test plug in wearbushing." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Halliburton prepared unit prior to testing." "On 2008-12-21, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Pressure tested BOP and IBOPs to 20/345 bar 5/10 min." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.8 hours. Operational details: Continued pressure testing BOP and IBOPs to 20/345 bar 5/10 min. Meanwhile changed spinner on aft iron roughneck and performed maintenace on same." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: PU test tool out of wear bushing and sat string in slips." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: RU to test IBOP and kelly hose." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Cleared rig floor of csg tong, PS30, inserts, bx-elevator, FMS, PADPRT and wear busing RT. Meanwhile performed test run on aft iron roughneck." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.8 hours. Operational details: Pressure tested TDS, lower- and upper IBOP and kelly hose to 30 bar/345 bar for 5/10 min. Meanwhile repaired CRI pumps and manifold. Cleaned threads on 5 1/2' DP on cantilever." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: RD test line to BOP. POOH and LD BOP test plug assembly. Meanwhile repaired CRI pumps and manifold. Cleaned threads on 5 1/2' DP on cantilever." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk. Serviced PRS. Inspected rollers and changed dies on PRS." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Held tool box talk for manual handling. LO 17 1/2' BHA." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Held time out for safety (TOFS). Had incident where lifting arrangement on lifting sub slipped and lifting sub dropped. Modified lifting arrangement and performed lifting/stress test. Ok." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Continued LO 17 1/2' BHA. Meanwhile repaired CRI pumps and manifold." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 75m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: PU and MU 12 1/4' BHA and RIH from surface to 75 m. Changed out master bushings to PS21." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 12 1/4' BHA from 75 m to 274 m. PS21 slips was locked in closed position." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Trouble shot mal function of PS21 slips." "On 2008-12-22, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held tool box talk prior to hanging of blocks." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Performed slip & cut of drill line." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Continued performing slip & cut of drill line." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Inspected aft PRS for dropped objects." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Serviced aft PRS and checked bolts on upper connection." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Serviced aft PRS and checked bolts on upper connection." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'drilling -- other' and lasted for 3.5 hours. Operational details: Completed Drops inspection on aft PRS. De-isolated equipment." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 274m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Changed faulty PS21 to PS30 slips and inserted correct carrier and inserts." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2480m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: RIH with 12 1/4' BHA from 274 m to 2480 m. Filled every 10 stds with 1.43 sg OBM." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2480m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: LO single and performed kick drill in 38 sek." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2521m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Broke circulation and washed down 12 1/4' BHA from 2480 m to 2521 m. Drilling parameters : 2000 lpm / SPP 62 bar / 30 RPM / torque 12-15 kNm." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2521m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed choke drill with day crew." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2534m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Broke circulation and washed down 12 1/4' BHA from 2521 m to 2534.4 m. Tagged cmt with 3 MT at 2534.4 m. Drilling parameters : 2000 lpm / SPP 62 bar / 30 RPM / torque 12-15 kNm." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2561m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled out shoe track from 2534.4 m to 2561 m whilst displacing to 1.25 sg. Drilling parameters : 3000 lpm / SPP 120 bar / 60 RPM / torque 15-17 kNm." "On 2008-12-23, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2561m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Dumped u-tube and flushed choke/kill and poorboy with 1.25 sg OBM. Filled trip tank and u-tube with 1.25 sg OBM. Liquid seal pressure on u-tube was 12 psi. Lined up manifolds and took SCR with 1.25 sg OBM. Made connection before cleaning out rat hole." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled out shoe track from 2561 m to 2562 m. Cleaned out 17 1/2' rat hole from 2562 m to 2591 m in 2-4 m increments and reamed. Drilling parameters : 3000 lpm / SPP 100 bar / 64 RPM / torque 15-17 kNm / WOB 1-2 MT. Observed aluminium swarf on shakers." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2560m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pumped OOH with 12 1/4' BHA from 2591 m to 2560 m and washed back down with 12 1/4' BHA from 2560 m to 2591 m. Parameters : 3000 lpm / SPP 103 bar / 64 RPM / torque 15-17 kNm. POOH with 12 1/4' BHA from 2591 m to 2560 m without rotation to verify no restriction in shoe track." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2567m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Positioned bit at 2567 m, and continued circulating hole clean. Parameters : 3000 lpm / SPP 103 bar / 30 RPM / torque 12 kNm." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Ran back to TD with 12 1/4' BHA and placed 5 m3 LCM pill from 2591 m to 2556 m (inside 13 3/8' csg shoe). Parameters : 660-3000 lpm / SPP 9-103 bar / 30 RPM / torque 12-13 kNm." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2547m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pulled bit slowly from 2591 m to 2547 m." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2547m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: RU TIW, pump-in sub and cmt hose. Meanwhile held tool box talk for FIT. Lined up for pumping down both drill pipe and kill line. Closed pipe ram on BOP. Verified line-up and performed line test to 100 bar/5 min. Ok." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2547m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Took FIT equivalent to 1.56 SG, using 1.25 SG OBM. Pumped 70 lpm and applied 76 bars to the string and annulus. Shut down the pump. Observed 0.5 bar drop (0.65%) in 6 min on FIT. Pressure levelled out. 1270 ltrs pumped and 1270 ltrs bled back." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2547m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Flow checked well for 15 min. Static. RD TIW, pump-in sub and cmt hose. Opened BOP pipe ram. Lined up for tripping." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA from 2547 m to 2581 m. Had 12 MT drag at 2581 m. MU TDS and washed down with 12 1/4' BHA from 2581 m to 2591 m. Parameters : 2000 lpm / SPP 50 bar / 30 RPM / torque 15-17 kNm. No obstruction observed. Meanwhile MU and checked gyro tools on main deck. PU and MU gyro tool on drill floor." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- survey' and lasted for 1.8 hours. Operational details: Installed battery and dropped gyro tool string inside DP. Pumped down tool with 500 lpm and landed gyro on totco ring at 2515.6 m. Parameters : 500 lpm / SPP 2 bar / 15 RPM / torque 14-17 kNm. Performed rotational shots and gyro tool QC at 2613 m. Accedently fired jar when starting to POOH. Evaluated situation for potential damage to gyro." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2560m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: POOH with 12 1/4' BHA from 2591 m to 2560 m. Meanwhile performed gyro survey on connection while POOH." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2560m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pumped 3.9 m3 1.50 sg slug at 880 lpm / 12 bar. Meanwhile held tool box talk prior to LO 5 1/2' DP in singles." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2546m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' BHA from 2560 m to 2546 m laying down 5 1/2' DP in singles." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2546m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Trouble shot HTS rollers." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2225m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH with 12 1/4' BHA from 2546 m to 2225 m RB 5 1/2' DP in derrick while continued trouble shooting of HTS rollers. Meanwhile performed gyro survey on connection while POOH." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2225m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Trouble shot draw works movement malfunction." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2225m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Trouble shot PDM malfunction." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1700m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: POOH with 12 1/4' BHA from 2225 m to 1081 m RB 5 1/2' DP in derrick while trouble shooting on PDM. Meanwhile performed gyro survey on connection while POOH. Performed rotational shots and gyro tool QC every 300 m." "On 2008-12-24, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1081m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: POOH with 12 1/4' BHA from 2225 m to 1081 m laying down 5 1/2' DP in singles. Meanwhile performed gyro survey on connection while POOH. Performed rotational shots and gyro tool QC every 300 m." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1081m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Investigated problem with HTS belt. Re-sat encoder" "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 189m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: POOH with 12 1/4' BHA from 1081 m to 189 m laying down 5 1/2' DP in singles. Meanwhile performed gyro survey on connection while POOH. Performed rotational shots and gyro tool QC every 300 m." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 12 1/4' BHA from 189 m to 84 m laying down 5 1/2' DP in singles. Meanwhile performed gyro survey on connection while POOH. Performed rotational shots and gyro tool QC every 300 m." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Removed gyro tool from string." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: MU and RB stnd of HWDP. Changed PS30 to master bushings. Meanwhile plugged gyro to computer to check quality of data." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH and LO 12 1/4' BHA from 84 m to OOH. Cleaned rig floor prior to RIH with 5 1/2' DP." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1009m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: RIH with 5 1/2' DP from surface to 1009 m." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.2 hours. Operational details: POOH and LO 5 1/2' DP to deck from 1009 m to 968 m. Pumped 3.5 m3 1.45 sg slug. Continued to POOH and LO 5 1/2' DP to deck from 968 m to OOH." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Cleaned and cleared rig floor. Re-arranged collars and landing string in derrick. BX-elevator would not close and tilt at the same time." "On 2008-12-25, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.8 hours. Operational details: Trouble shooted BX-elevator." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Continued trouble shooting BX-elevator." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 856m. The activity was categorized as 'drilling -- trip' and lasted for 5.2 hours. Operational details: PU and RIH with 'new' 5 1/2' DP from surface to 856 m." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1894m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: PU and RIH with 'new' 5 1/2' DP from 856 m to 1894 m in singles from deck." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Pumped 3 m3 1.49 slug. POOH and RB 5 1/2' DP in derrick from 1894 m to surface." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Cleaned and cleared drill floor. Removed PS30 and installed master bushings. Prepared rig floor for 8 1/2' BHA." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: PU 8 1/2' BHA and RIH from surface to 42 m. Loaded sources into MWD tool. Continued PU 8 1/2' BHA and RIH from 42 m to 99 m. Performed recalibration of block weight sensor while waiting on helicopter for 10 min." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 505m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Dressed and installed PS21 slips and checked dies on PRS. RIH with 8 1/2' BHA on 5' DP from 99 m to 584 m drifting every stnd of 5' DP to 3.0' in derrick." "On 2008-12-26, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 505m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Installed XO and filled pipe. Broke circulation and pumped 2000 lpm / 80 bar." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 505m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed shallow test of Schlumberger tools at 2000 lpm / 80 bar. Ok" "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1728m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 505 m to 1727 m drifting every stnd of 5' DP to 3.0' in derrick. Filled pipe every 15 stnds." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1728m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Isolated and serviced TDS." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1728m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Isolated and serviced aft PRS." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1728m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2495m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: RIH with 8 1/2' BHA from 1728 m to 2495 m PU 5 1/2' DP from deck." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2535m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' BHA from 2495 m to 2535 m on 5 1/2' DP from derrick." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2593m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: MU TDS and filled pipe. Washed down with 8 1/2' BHA from 2535 m to 2593 m on 5 1/2' DP from derrick. Parameters : 1600 lpm / SPP 80 bar / 50 RPM / torque 7-9 kNm." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 8 1/2' hole from 2593 m to 2596 with 1.25 sg OBM . Drilling parameters : 1800-2000 lpm / SPP 102-120 bar / 50-80 RPM / torque 9-12 kNm / WOB 1-3 MT / ECD 1.27 sg EQMW. Up weigh 154 MT / Rotational weight 135 MT / Down weight 128 MT." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2594m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Picked off btm to take survey. Observed pressure spike of 15 bar. Attempted to come back down but took weight at 2594 m. Observed pressure increase. Reamed stand and cleaned hole. Attempted to come back down with 1800 lpm / 50 rpm but took weight at 2594 m. Observed pressure increase of 35 bar. Observed no increase in torque, and no reduction in return flow. Sat down 10 MT WOB and continued to observe pressure increase of 30 bar, not possible to come back to btm. Observed decrease in torque from 8-10 kNm to 6-7 kNm, no reduction in return flow observed." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2576m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: POOH with 8 1/2' BHA from 2594 m to 2576 m and circulated while discussing options. Parameters : 1800 lpm / SPP 96 bar / 10 RPM / torque 7-9 kNm." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2549m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH from 2576 m to inside 13 3/8' csg shoe at 2549 m. Performed flow check of well while discussing options with town. Static." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1728m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Pumped 3.5 m3 1.50 sg slug at 1000 lpm / 36 bar. POOH with 8 1/2' BHA from 2549 m to 1728 m on 5 1/2' DP." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1727m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: LO XO and changed to 5' handling equipment." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 8 1/2' BHA from 1727 m to 100 m on 5' DP." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well. Static. Meanwhile removed PS21 slips and installed master bushings." "On 2008-12-27, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Continued to POOH with 8 1/2' BHA from 100 m to 30 m." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: De-activated batteries in Sonic Vision Tool. Torque tested 6.5' jar to 20 kNm both left and right hand turn. Ok." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Continued to POOH with 8 1/2' BHA from 30 m to OOH. Removed radio active source from Ecoscope. Inspected bit and Xceed. Ok. Torque tested bit shaft on Xceed to 17 kNm. No movement observed." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Broke 8 1/2' bit from Xceed. Broke out Xceed on the btm sub of the Ecoscope by mistake." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Broke out another sub on the Ecoscope and made up a connection by hand to not damage the extender." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Broke out and LO the Xceed. PU backup Xceed and MU to 8 1/2' PDC bit. MU Ecoscope and inserted radioactive source. MU and RIH with Sonic Vison and Stetoscope to 42 m and re-activated batteries." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Changed elevator inserts to 5'. PU and RIH with backup 6.5' drilling jar to 70 m. Continued PU 8 1/2' BHA and RIH from 70 m to 99 m." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 303m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Dressed and installed PS21 slips. RIH with 8 1/2' BHA on 5' DP from 99 m to 303 m." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 506m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 303 m to 506 m." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 506m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Installed XO and filled pipe. Broke circulation and pumped 2000 lpm / 80 bar." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 506m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Performed shallow test of Schlumberger tools at 2000 lpm / 80 bar. Ok. Meanwhile held tool box talk for RIH." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2374m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 506 m to 1727 m. Changed to 5 1/2' handling equipment and RIH with 8 1/2' BHA on 5 1/2' DP from 1727 m to 2374 m. Filled pipe every 15 stnds." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2374m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Investigated why BX-elevators opened without command. Changed out BX-elevator." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2534m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 2374 m to 2534 m. Filled pipe every 15 stnds." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2595m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: MU TDS and filled pipe. Washed down with 8 1/2' BHA from 2534 m to 2595 m on 5 1/2' DP from derrick. Parameters : 1600 lpm / SPP 75 bar / 50 RPM / torque 9-11 kNm. Up weigh 150 MT / Rotational weight 138 MT / Down weight 128 MT. Lined up manifold to one stand pipe due to noise in mud signal. Took survey. Tagged 2595 m and observed 15 bar pressure increase." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2603m. The activity was categorized as 'drilling -- ream' and lasted for 1.2 hours. Operational details: Reduced flow and attempted to come down. Parameters : 1100 lpm / SPP 41 bar / 50 RPM / torque 9-11 kNm. Tagged 2595 m and observed 30 bar increase in pressure. Pressure dropped back to 41 bar after 1 m drilled. Drilled 8 1/2' hole from 2595 m to 2603 with 1.25 sg OBM . Drilling parameters : 1100 lpm / SPP 41 bar / 50 RPM / torque 16-18 kNm / WOB 8 MT / ECD 1.27 sg EMW. Observed torque increase and WOB fluctuate from 6-12 MT when stabilizers passed 2595 m. Continued drilling 8 1/2' hole from 2603 m to 2616 with 1.25 sg OBM . Drilling parameters : 2000 lpm / SPP 123 bar / 80 RPM / torque 12-15 kNm / WOB 4-7 MT / ECD 1.28 sg EMW." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2604m. The activity was categorized as 'drilling -- ream' and lasted for 0.8 hours. Operational details: Reamed back from 2616 m to 2600 m before taking connection. Parameters : 2000 lpm / SPP 123 bar / 80 RPM / torque 12-15 kNm. No obstruction observed. RIH with no rotation to verify stabilizers were clear. POOH to 2590 m while pumping 200 lpm / 1 bar. RIH and took 8 MT drag at 2595 m. PU to 2590 m and washed down to 2604 m without obstructions. Parameters : 1000 lpm / SPP 30 bar / 50 RPM / torque 8-10kNm." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2614m. The activity was categorized as 'drilling -- ream' and lasted for 2.2 hours. Operational details: Reamed back from 2604 m to 2594 m. Parameters : 2000 lpm / SPP 118 bar / 80 RPM / torque 8-10 kNm. Attempted to RIH to TD but observed obstruction at 2610 m. Reduced flow and attempted to get past obstruction. Parameters : 1100 lpm / SPP 41 bar / 50 RPM / torque 7-10 kNm. Observed 35 bar pressure increase and WOB increased while TDS was stationary (pack-off). PU above obstruction and changed flow/rotation. Parameters : 1800 lpm / SPP 100 bar / 120 RPM / torque 6-12 kNm. Worked past obstruction to 2614 m." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- ream' and lasted for 3.5 hours. Operational details: Worked past obstruction at 2614 m and tagged TD at 2616 m. Parameters : 1800 lpm / SPP 100 bar / 120 RPM / torque 6-12 kNm. Reduced string rotation to 80 RPM and reamed from 2616 m to 2576 m. While reaming down took weight at 2596 m and observed pressure of 15 bar. Worked past tight spots to 2516 m." "On 2008-12-28, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated hole clean while reaming from 2616 m to 2610 m (all tools in open hole). Parameters : 2150 lpm / SPP 130 bar / 140 RPM / torque 8-10 kNm. Observed red fiber-glass material and swarf coming over the shakers." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Continued circulating hole clean while reaming from 2616 m to 2610 m (all tools in open hole). Parameters : 2150 lpm / SPP 130 bar / 140 RPM / torque 8-10 kNm. Observed red fiber-glass material and swarf comming over the shakers. A total of 2 btms up pumped." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Attempted to pump slug pill from pit #8, but due to lighter fluid on suction end, the pill had to be transfered to pit #15 before it was pumped downhole. Meanwhile continued to circulate with reduced rate (1800 lpm) while transfering pill." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Pumped 5 m3 1.525 sg visc slug pill and circulated out same. Parameters : 2150 lpm / SPP 130 bar / 140 RPM / torque 8-10 kNm. Observed increased returns, red fiber-glass material and swarf comming over the shakers." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Reduced string rotation to 80 RPM and reamed from 2616 m to 2576 m and back down again. Parameters : 2150 lpm / SPP 130 bar / 80 RPM / torque 8-10 kNm. Worked pipe slightly on last 3 m above TD." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2610m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: POOH from 2616 m to 2576 m and back down again. Parameters : 880 lpm / SPP 25 bar. While RIH took weight at 2594 m. Worked past several tight spots down to 2510 m and observed pressure spikes of 38 bar." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2610m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 5 m3 1.525 sg visc slug pill at 900 lpm and started to circulate out same. Parameters : 2150 lpm / SPP 130 bar / 140 RPM / torque 8-10 kNm." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2615m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated out 5 m3 1.525 sg visc slug pill whilst reaming from 2615 m to 2576 m. Parameters : 2150 lpm / SPP 130 bar / 80-140 RPM / torque 8-10 kNm. Up weigh 152 MT / Rotational weight 136 MT / Down weight 128 MT." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2615m. The activity was categorized as 'drilling -- ream' and lasted for 3.0 hours. Operational details: Continued circulating whilst reaming from 2575 m to 2606 m. Worked to pass obstruction at 2606 m and continued to ream down to 2615 m. Parameters : 2150 lpm / SPP 130 bar / 80-140 RPM / torque 8-10 kNm. Reamed down to TD and observed no pressure peaks or WOB. Simulated connection and took survey." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2656m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Made connection and drilled 8 1/2' hole from 2616 m to 2656 m with 1.25 sg OBM . Drilling parameters : 2150 lpm / SPP 130 bar / 140 RPM / torque 12-16 kNm / WOB 2-3 MT / ECD 1.28 sg EMW." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2656m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Reamed from 2656 m to 2616 m while circulating btms up. Parameters : 1600 lpm (down)-2150 lpm (up) / SPP 78 bar (down)-130 bar (up) / 60 RPM (down)-140 RPM (up) / torque 7-11 kNm (down) 8-10 kNm (up)." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2656m. The activity was categorized as 'drilling -- ream' and lasted for 2.2 hours. Operational details: Pumped OOH from 2616 m to 2576 m. Reamed back in the hole to 2626 m. Worked to pass obstruction at 2626 m. Pressure increased with 30 bar. Continued to ream down to 2656 m. Parameters : 2150 lpm / SPP 130 bar / 80-140 RPM / torque 8-10 kNm. Took SCRs and made connection." "On 2008-12-29, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2777m. The activity was categorized as 'drilling -- drill' and lasted for 7.8 hours. Operational details: Drilled 8 1/2' hole from 2656 m to 2777 m with 1.25 sg OBM . Drilling parameters : 2150 lpm / SPP 130 bar / 140 RPM / torque 12-13 kNm / WOB 3-6 MT / ECD 1.29 sg EMW / ROP 20-30 m/hr." "On 2008-12-30, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2818m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 8 1/2' hole from 2777 m to 2818 m with 1.25 sg OBM in Ty. Drilling parameters : 2150 lpm / SPP 138 bar / 140-160 RPM / torque 12-15 kNm / WOB 3-4 MT / ECD 1.29 sg EMW / ROP 30 m/hr." "On 2008-12-30, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2889m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 8 1/2' hole from 2818 m to 2889 m with 1.25 sg OBM in Shetland . Drilling parameters : 2150 lpm / SPP 138 bar / 140-200 RPM / torque 16-17 kNm / WOB 6-10 MT / ECD 1.29-1.30 sg EMW / ROP 15-30 m/hr." "On 2008-12-30, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3059m. The activity was categorized as 'drilling -- drill' and lasted for 11.2 hours. Operational details: Drilled 8 1/2' hole from 2889 m to 3059 m. Started to increase MW from 1.25 sg to 1.32 sg at 2920 m whilst drilling ahead. Drilling parameters : 2150 lpm / SPP 148 bar / 130-180 RPM / torque 15-20 kNm / WOB 7-10 MT / ECD 1.36-1.37 sg EMW / ROP 20-30 m/hr. Meanwhile worked on aft PRS to be able to MU and RB 10 3/4' csg." "On 2008-12-30, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3059m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Circulated cuttings clear off 8 1/2' BHA. Parameters : 2150 lpm / SPP 150 bar / 150 RPM / torque 11-12 kNm. Took SCRs on MP1 and MP#." "On 2008-12-30, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3095m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Circulated hole clean whilst investigating problem with PRS bladder on lower arm." "On 2008-12-30, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3142m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole from 3059 m to 3142 m in Shetland with 1.32 sg OBM. Drilling parameters : 2100-2150 lpm / SPP 144-152 bar / 150 RPM / torque 16-20 kNm / WOB 8-15 MT / ECD 1.37 sg EMW / ROP 5-30 m/hr. Meanwhile prepared for MU and RB 10 3/4' csg. Had to use emergency stop on HTS to stop 10 3/4' csg joint which was moved too far forward and tilted onto drill flor. Investigated problem and recalibrated HTS joy stick." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3155m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 8 1/2' hole from 3059 m to 3142 m in Shetland with 1.32 sg OBM. Drilling parameters : 2150 lpm / SPP 145 bar / 160 RPM / torque 15-19 kNm / WOB 11-15 MT / ECD 1.35 sg EMW / ROP 2-5 m/hr. Meanwhile started to MU and RB stands of 10 3/4' csg in derrick. A 10 3/4' csg double slided out of grip when aft PRS was transfering/lifting casing out of double latch at set back. The 10 3/4' csg double fell on to TDS blower hose." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3155m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Evaluated situation. Made SJA and held tool box talk for recovering 10 3/4' csg double. Secured lower end of csg and attached pick up elevator on top end. Meanwhile circulated 8 1/2' hole at minimum rate. Parameters : 1100 lpm / SPP 42 bar / 60 RPM / torque 10-12 kNm. Stopped rotation when man-riding to attach pick up elevator." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3155m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Made SJA and held tool box talk for recovering 10 3/4' csg double. Secured lower end of csg and attached pick up elevator on top end. Hoisted csg vertical and secured in aft PRS. Inspected TDS blower hose for damage. Ok. Meanwhile circulated 8 1/2' hole at minimum rate. Parameters : 1100 lpm / SPP 42 bar / 60 RPM / torque 10-12 kNm. Stopped rotation when man-riding to attach pick up elevator." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: Drilled 8 1/2' hole from 3142 m to 3180 m in Shetland with 1.32 sg OBM. Drilling parameters : 2150 lpm / SPP 146 bar / 160-200 RPM / torque 14-18 kNm / WOB 9-12 MT / ECD 1.34-1.35 sg EMW / ROP 2-9 m/hr. Stopped pumps to reset BHA tools. Not able to build angle/no response from Xceed. Decided to POOH to change BHA." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated btms up at and took survey. Parameters : 2150 lpm / SPP 146 bar / 170 RPM / torque 11-12 kNm." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well on trip tank. Ok. Meanwhile held tool box talk for POOH." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2980m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' drilling BHA wet from 3180 m to 2980 m. Had 20 MT overpull from 3000 m to 2980 m and observed improper hole displacement of 300 ltrs." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' drilling BHA back to btm from 2980 m to 3180 m." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- trip' and lasted for 4.8 hours. Operational details: Pumped OOH with 8 1/2' drilling BHA from 3180 m to 2536 m at 1000 lpm / 37 bar. - Observered 25 bar increase in SPP at 2748 m. Reduced pumps and worked pipe. - Observered 20 bar increase in SPP at 2685 m and took weight. Reamed out stand with 10 rpm." "On 2008-12-31, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Circulated btms up inside 13 3/8' csg shoe. Parameters : 2150 lpm / SPP 139 bar. Meanwhile serviced TDS and aft PRS." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued circulating btms up inside 13 3/8' csg shoe. Parameters : 2150 lpm / SPP 139 bar. Meanwhile serviced TDS and aft PRS." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well. Stable." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 5 m3 1.57 sg slug." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Changed BX-elevator." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1933m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 8 1/2' drilling BHA from 2536 m to 1933 m. Had to reset SBC for aft iron roughneck." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1933m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Investigated and repaired hydraulic leak on hose in cable tray on aft PRS drag chain in derrick." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1933m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Changed leaking hydraulic hose in cable tray on aft PRS drag chain in derrick. Meanwhile function tested BOP and flushed choke & kill lines. De-isolated and function tested aft PRS." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1743m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 8 1/2' BHA from 1933 m to 1728 m on 5 1/2' DP." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1743m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: LO XO and changed to 5' handling equipment." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 8 1/2' BHA from 1743 m to 140 m on 5' DP." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Flow checked well. Static. Removed PS21 slips and installed master bushings. Meanwhile changed out BX-elevator." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued to POOH with 8 1/2' BHA from 140 m to 43 m. At 13:00 hrs held tool box talk and sat back stnd of 5' HWDP that came out of fingerboard during racking." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Removed radio active source from Ecoscope. Broke out and LD MWD tools and Xceed." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk prior to PU new 8 1/2' drilling BHA. Meanwhile functioned shear rams and cleaned & cleared rig floor." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 42m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: PU backup Xceed and MU to new 8 1/2' PDC bit. Downloaded data from Ecoscope. MU Ecoscope and inserted radioactive source. MU and RIH with Sonic Vison and Stetoscope to 42 m and activated new batteries. Meanwhile cleaned drill floor and shaker areas." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Changed elevator inserts to 5'. RIH with 8 1/2' BHA from 42 m to 99 m." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 588m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Dressed and installed PS21 slips. RIH with 8 1/2' BHA on 5' DP from 99 m to 588 m." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 588m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Installed XO and filled pipe. Broke circulation and pumped 1800 lpm / 69 bar. Performed shallow test of Schlumberger tools. Ok. Meanwhile lifted CTS funnel from template with crane to main deck for inspection." "On 2009-01-01, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 588 m to 1077 m." "On 2009-01-02, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: RIH with 8 1/2' BHA on 5' DP from 1077 m to 1726 m. Changed to 5 1/2' handling equipment and RIH with 8 1/2' BHA on 5 1/2' DP from 1726 m to 2532 m. Filled pipe every 15 stnds." "On 2009-01-02, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: MU TDS and filled pipe. Staged up pumps and circulated btms up at 13 3/8' csg shoe at 2532 m. Parameters: 2150 lpm / bar." "On 2009-01-02, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2635m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH with 8 1/2' BHA from 2532 m to 2594 m. Found obstruction at 2594 m. PU 1-2 m and washed down stand. Continued RIH with 8 1/2' BHA from 2594 m to 2630 m. Found obstruction at 2630 m. PU 1-2 m and washed down stand. Parameters : 1600 lpm / SPP 80 bar / 50 RPM / torque 9-11 kNm. Up weigh 150 MT / Rotational weight 137 MT / Down weight 128 MT." "On 2009-01-02, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3141m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Continued RIH with 8½' BHA from 2636m to 3141m. Took weight at 2668m and 2696m. Reamed through with 2000 lpm and 50/60 rpm." "On 2009-01-02, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3181m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Made up to TDS and washed down last stand from 3141m to 3180m, with 2000 lpm, 60 rpm. Drilled 1 meter to 3181m before taking connection." "On 2009-01-02, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3342m. The activity was categorized as 'drilling -- drill' and lasted for 10.2 hours. Operational details: Continued drilling 8½' hole from 3181 m to 3342 m. Flow 2100 lpm / SPP 148 bars / String RPM 120 TQ 8-29 kNm / WOB 8-10 / ECD 1.36 EMW / MUD weight 1.32 SG / ROP 19-21mph. Up weight 170 MT / Down weight 132 MT / Free rotational weight 147 MT. Parallel activity: Made up 10-3/4' CSG in std and rack back in derrick." "On 2009-01-02, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3385m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Continued drilling 8½' hole from 3342 m to 3385 m. Flow 2100 lpm / SPP 148-150 bars / String RPM 120 TQ 12-30 kNm / WOB 5-8 / ECD 1.36-1.38 EMW / MUD weight 1.32-1.34 SG / ROP 20 mph. Up weight 172 MT / Down weight 128 MT / Free rotational weight 147 MT. Weighted up mud to 1.34 SG. Parallel activity: Made up 10-3/4' CSG in std and rack back in derrick." "On 2009-01-03, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3481m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 8½' hole from 3385 m to 3481 m. Flow 2100 lpm / SPP 150 bars / String RPM 120 TQ 13-32 kNm / WOB 5-10 / ECD 1.38-1.39 EMW / MUD weight 1.34 SG / ROP 20 mph. Up weight 173 MT / Down weight 132 MT / Free rotational weight 146 MT. Parallel activity: Made up 10-3/4' CSG in std and rack back in derrick. Status: 11 std in derrick." "On 2009-01-03, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3829m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Continued drilling 8½' hole from 3481 m to 3829 m. Flow 2100 lpm / SPP 150-160 bars / String RPM 120-160 TQ 13-32 kNm / WOB 5-10 / ECD 1.39-1.41 EMW / MUD weight 1.34 SG / ROP 20-32 mph. Up weight 184 MT / Down weight 135 MT / Free rotational weight 152 MT. Parallel activity: Made up 10-3/4' CSG in std and rack back in derrick. Status: 18 std in derrick. Unable to continue with making up 10-3/4' CSG in std, due to male function of HTS. Started to repair same." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3866m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 8½' hole from 3829 m to 3866 m. Flow 2100 lpm / SPP 160 bars / String RPM 160 TQ 19-27 kNm / WOB 2-8 / ECD 1.41 EMW / MUD weight 1.34 SG / ROP 20-32 mph. Up weight 185 MT / Down weight 135 MT / Free rotational weight 154 MT. Parallel activity: Continued with trouble shoot of HTS." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3866m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated hole clean prior to take pressure points, reciprocating the string. Simultaneously held tool box talk prior to take pressure points." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3866m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Performed sticky test. Correlation log from 3832m to 3842m. Took pressure points: MD probe TVD Reservoir press. Mud hydrostatic Pressure gradient 3802m 3001.5m 318.7 bars 410.7 bars 1.08 SG 3811m 3007.5m 319.3 bars 411.8 bars 1.08 SG 3831m 3021.0m 320.8 bars 412.8 bars 1.08 SG" "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3915m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued drilling 8½' hole from 3866mto 3915 m. Flow 2100 lpm / SPP 160-163 bars / String RPM 160 TQ 18-21 kNm / WOB 8-12 / ECD 1.40-1.41 EMW / MUD weight 1.34 SG / ROP 32 mph. Up weight 184 MT / Down weight 135 MT / Free rotational weight 152 MT." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3947m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued drilling 8½' hole from 3866 m to 3947 m. Flow 2100 lpm / SPP 164 bars / String RPM 126 TQ 19-26 kNm / WOB 7-8 / ECD 1.41 EMW / MUD weight 1.34 SG / ROP 25-35 mph. Up weight 190 MT / Down weight 136 MT / Free rotational weight 152 MT." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3947m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated hole clean prior to take pressure points, reciprocating the string, 1800lpm 80 rpm. Performed sticky test." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3947m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Took pressure points: MD probe TVD Reservoir press. Mud hydrostatic Pressure gradient 3882m 3054.6m 324.4 bars 416.9 bars 1.083 SG 3860m 3039.7m 322.7 bars 414.9 bars 1.082 SG 3849m 3032.4m 321.9 bars 413.9 bars 1.082 SG" "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4027m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Continued drilling 8½' hole from 3947 to 4027 m. Flow 2100 lpm / SPP 163 bars / String RPM 160 TQ 19-26 kNm / WOB 7-8 / ECD 1.42 EMW / MUD weight 1.34 SG / ROP 25-35 mph. Up weight 192 MT / Down weight 139 MT / Free rotational weight 159 MT. Took survey at 3947m. Parallel activity: MU 10 3/4' casing and racked in derrick. Status: 22 stands racked back." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4027m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated hole clean prior to take pressure points, reciprocating the string, 2100lpm 160 rpm. Performed sticky test." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4027m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Took pressure points: MD probe TVD Reservoir press. Mud hydrostatic Pressure gradient 3963.5m 3111.6m 359.1 bars 428.2 bars 1.176 SG 3981m 3125.0m 347.2 bars 429.2 bars 1.133 SG 3977m 3067.1m 347.8 bars 428.2 bars 1.135 SG" "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4095m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Continued drilling 8½' hole from 4027 to 4095 m. Flow 2100 lpm / SPP 163 bars / String RPM 160 TQ 19-26 kNm / WOB 7-8 / ECD 1.42 EMW / MUD weight 1.34 SG / ROP 25-35 mph. Up weight 192 MT / Down weight 139 MT / Free rotational weight 159 MT. Took survey at 4075m." "On 2009-01-04, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4095m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.8 hours. Operational details: Circulated well clean while reciprocating the drill string, 2100 lpm, 164 bars and 160 rpm. After 1 BU pumped 5.5m³ 1.60 SG Hi-vis pill. Simultaneously rigged up wire line prior to run VSP." "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4095m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.8 hours. Operational details: Continued circulated well clean reciprocating the drill string, 2100 lpm, 164 bars and 160 rpm. Conditioned mud from 1.35+ SG to 1.34 SG. Redused mixing capacity due to break down / availability of centrifuge and mixing pumps. Meanwhile RU WL equipment in derrick and V-door." "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4095m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Took up/down weight 200/145 MT neautral wt 164 MT. Performed flow check - well static. Simultaneously 15 min. sticky test, Pick up weight 212 MT to free movement. Held tool box talk prior to RU CSES. Performed 30 min. sticky test, Pick up weight 218 MT to free movement" "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4082m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: RIH and tagged TD at 4095m. PU to 4082 m. RU for WL." "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- survey' and lasted for 3.8 hours. Operational details: Installed master bushing. Made up VSP logging tools and CSES and tested VSP logging tool string. Took pick up weight of DP string 210 MT and down 139 MT." "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Held tool box talk prior to RIH with VSP logging string." "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- survey' and lasted for 4.8 hours. Operational details: RIH with VSP logging tools on wire line as per program, Maded several attempts to pump down. 680lpm = 27 bar, 900lpm = 38 bar, 1100lpm = 60 bar, 1200 lpm 64 bar, 1300lpm = 73 bar, 1400lpm = 86.6 bar Time picked up string & broke over with 09.45 = 210 up, 144 down MT 12.45 = 215 up, 144 down MT 15.15 = 226 up, 144 down MT 16.15 = 220 up, 144 down MT 17.45 = 216 up, 144 down MT" "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'formation evaluation -- log' and lasted for 8.8 hours. Operational details: Started VSP logging while POOH as per Schumbergers logging depths. From 3995 m and every 15 meters to 986m. Time picked up string & broke over with 1915 = 214 up, 145 down MT 2100 = 222 up, 145 down MT 2230 = 223 up, 145 down MT 2345 = 220 up, 145 down MT" "On 2009-01-05, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: POOH with WL from 986m to 450m." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- survey' and lasted for 2.8 hours. Operational details: Continued POOH with WL from 450m to surface. Held tool box talk and RD CSES, LO VSP logging String and Schlumburger WL equipment, LO X-overs." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated BU 2100 lpm, 170 bars, 160 rpm. Meanwhile RD WL on the rig floor, V door and the cantilever." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held tool box talk and assemblied the Gyro data tool, waited for gyro to warm up to 40 degrees to check if working - not working." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Changed batteries in gyro tool." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Dropped Gyro and pumped down same as per Gyro-data instructions, 375 lpm and 1100 lpm. Torque off bottom = 13 - 18 kNm Meanwhile install PS21 auto slips." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Down linked sonic tool as per instructions." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4093m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH to 4093 m took up/down weight 210/144 MT, followed gyro instructions, took rotation shots." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4093m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well - well static." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3300m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: POOH pumping, from 4093 m @ 1000 lpm, Took rotation shots @ 3784m to 3343m. Pulling speed 198 m/hours. ESD shut down on production." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3300m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: ESD shut down on production, Waited on electrician to reset equipment on drill floor." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Continued to pump out of hole from 3300m, took rotation shots @ 3180m to 2536m inside shoe. Pulling speed 173 m/hours. Evacuated rig floor due to exhaust fumes entering rig floor. Continued reporting on F-99." "On 2009-01-06, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated bottom up from manual controls in pump room, 1950 lpm 129 bars. Continued reporting on F-99." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Held tool box talk and change PS21 to manual slips. Installed TIW. Retracted the block, lowered work platform." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Held tool box talk and changed out wash pipe. Pressure tested wash pipe to 200bars using rig pumps, re-tighten wash pipe." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Held tool box talk and attempted to rack back TDS work platform. Evacuated rig floor due to exhaust fumes entering rig floor. Continued reporting on F-99." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- repair' and lasted for 6.2 hours. Operational details: Held tool box talk and changed out hydraulic valve on TDS. Secured work platform." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Made up string to the TDS. Pump 5m³ of 1.60 SG slug. Chased same and allowed to settle." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Installed PS21 auto slips and pipe wiper." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1728m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH with 8½' BHA from 2531m to 1728m. Pulling speed 1144 m/hours." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1728m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Changed out handling gear from 5½' to 5'. Broke off X-over." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued POOH with 8½' BHA from 1728m to 140m. Pulling speed 794 m/hours." "On 2009-01-07, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well on trip tank prior to pulling BHA - well static." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pulled last stand of 5' DP out to 99m." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 7m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: POOH and broke out, laid down BHA. Replaced jar, removed Gyro, Totco and radio active source. Continued reporting on F-99" "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued brake out BHA and Bit. Bit gauged OK." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleared and cleaned drill floor." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: RIH with jetting sub and test plug from surface to 149m and jet washed the well head, 2000 lpm, 10 rpm." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Landed off test plug." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Installed swedge & hose to TDS prior to pressure testing." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.0 hours. Operational details: Held tool box talk and performed BOP pressure test 20/345 bars 5/10 min. Simultaneously pressure tested IBOP, Choke & Kill manifold 20/345 bars 5/10 min." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: POOH with BOP test plug. L/O test plug & pump in sub." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Cleared & cleaned rig floor." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Held tool box talk and rigged up to RIH w. 3½' cement singer/DP. To long delay time in tilt function of the BX elevators." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Changed out elevators to eliminate delay on tilt function." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk and RIH with 3½' cement singer/DP. Picked up 3½' DP from cantilever and ran in singles. Elevator not operating properly." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Removed inserts in elevators and checked activating pin." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.8 hours. Operational details: Continued RIH with 3½' cement singer/DP, from surface to 300m. Picked up 3½' DP from cantilever and ran in singles. Tripping speed 110 m/hours." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 302m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Changed out handling equipment from 3½' to 5'." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 912m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Continued RIH on 5' DP from 302m to 912m. Tripping speed 813 m/hours" "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 912m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Installed X/O and made up to TDS and broke circulation." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1524m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Continued RIH on 5' DP from 912m to 1524m. Tripping speed 612 m/hours." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1524m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Installed X/O and made up to TDS and broke circulation." "On 2009-01-08, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1890m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued RIH on 5' DP from 1524m to 1890m. Tripping speed 732 m/hours." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2011m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Continued RIH on 5' DP from 1890m to 2011m. Tripping speed 484 m/hours." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2011m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed handling equipment to 5½'." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2011m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Made up to TDS and broke circulation." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2537m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Continued RIH on 5½' DP from 2011m to 2537m. Tripping speed 701 m/hours." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2537m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Serviced TDS prior to entering shoe." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2609m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Continued RIH from 2537m-2609m. At 2609m tag obstruction with 5-8 MT." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2537m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Made up TDS to string and attempted to wash down. Observed pressure rise to 85 bars. Pulled back to 2578m and attempted to circulate. Immediately pressure increased to 44 bars. Monitor for pressured leak off - no pressure drop observed. Pulled to 2551m and attempted to circulate. Pressured up to 110bars. Pulled to 2537m and attempted to circulate. Confirmed string plugged by circulating through TDS and down mud bucket line." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2537m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: At 2537m, M/U TDS. Rotated string at 100rpm while applying pressure in 50bars increments. At 220bars pressure dropped off to 60bars. Increased flow rate and took roadmap pressures verses flow readings." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2656m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Washed down from 2537m to 2656m. 20 rpm, 6-9kNM torque, 69-92bar" "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2860m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Continued RIH with 5½ DP washing down 1000 lpm 20 rpm. From 2820m to 2860m." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3021m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Continued RIH from 2860m to 3021m. Broke circulation after 5 stds at 2981m. Took weight at 2999m, increased rate to 1000lpm, 20rpm. Continued to RIH without washing down from 3021m to 3142m." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4097m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.5 hours. Operational details: Took weight at 3142m take weight, increased rate to 1000lpm 20rpm. Continued to wash hole from 3142m to 4097m 1000lpm 20rpm. Tagged bottom at 4097m." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4092m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.5 hours. Operational details: Picked up 5m and conditioned to even mud weight 1.35 SG, 2000 lpm. Simultaneously held tool box talk prior to perform cement job." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4092m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pressure tested line from cement unit to standpipe manifold, 200bars." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4092m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 7m³ 1.60 SG spacer, chased with 2,6m³ OBM, 30 rpm & 14 kNm." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4092m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 9.45m³ 1,90 SG Silica cement slurry at 800 lpm. 50bars, 20 rpm & 14 kNm." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 4092m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Displaced cement with rig pumps 36.9m³ 2000 lpm 30 rpm." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3923m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH from 4092m to 3923m. Pulled wet." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3923m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: M/U TDS and circulated bottoms up at 2000lpm, 179bars. Observed cement in returns." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3923m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 7 m³ of 1.6 SG spacer. Chased with 2.6 m³ of 1.35 OBM. 30 rpm, 800 lpm, 14-16kNm." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3923m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Mixed and pumped 9.5 m³, 1.90 SG cement slurry, 800 lpm, 50 bar, 30 rpm and 14 kNm. ( 1st plug, 2nd stage)." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3923m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Displaced cement with 34.98 m³ 1.35 SG mud at 2000 lpm, 70 rpm, after 290 stks pressure increased from 0 to 129 bars - 146 bars." "On 2009-01-09, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3700m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: POOH from 3923m to 3700m. Pulled wet." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3670m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Continued POOH from 3700m to 3670m. Pulled wet." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3670m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: M/U TDS pumped 1 m³ to clear 3½' DP." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3630m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Continued POOH from 3670m to 3630m. Pulled wet." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3630m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Inserted 2 sponge balls into string and circulated balls down string with 51.2 m³ 1.35 SG mud. 2000 lpm, 170-190bars, 120 rpm, 14-16kNm." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3630m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Flushed manifold from cement unit to rig floor standpipe." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3630m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Pumped 18 m³ of Hi-vis 1.34 SG pill. Spotted on bottom with 35.76m³ 1.35 SG mud (1630 stks). 2000 lpm, 160-191bars." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3330m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH from 3630m to 3330m. Pulled wet." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3330m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Made up TDS. Circulated bottoms up at 2000 lpm, 158bars, 20rpm, 9-12kNM. Reduced flow rate to 1000 lpm at bottoms up to be able to detect Hi-vis pill over shakers." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3330m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Continued circulate 2000 lpm, 158bars, 20rpm, 9-12kNM. Verified Hi-vis pill in returns in pit room." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3330m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Held tool box talk and loaded Halliburton CST. Simultaneously conditioning the mud in pump room." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3329m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped down CST at 1000 lpm, 51.2 bars for 1331 stks, reduced rate to 500 lpm. Total 1403 stks. Simultaneously held tool box prior cement job. Pick up 1m from 3330m to 3329m." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3328m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Lined up cement unit to standpipe manifold and verify line up. Pumped 9m³ 1.60 SG spacer, chased with 2,6m³ OBM, 30 rpm & 14 kNm. 400 - 1000 lpm, 50 - 95 bars. Picked up 1m from 3329m to 3328m." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3328m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Mixed and pumped 11m³ 2.00 SG Norcem cement slurry at 800 lpm. 50bars, 30 rpm & 12 kNm. Displaced cement lines to rig floor." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3328m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Displaced cement plug with rig pumps 2000lpm, 120rpm, max 180bars, 28.06m³ pumped. Pressure seen on standpipe manifold after 7m³ pumped." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3080m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: POOH from 3328m to 3080m and pumped 1m³ to clear 3½' DP, pulling speed 3 min a stand. The 3 first connection was dry." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2760m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH from 3080m to 2760m. Pulling speed 640 m/hours." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2760m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Inserted 2 sponge balls into string and circulated bottoms up with 1.35 SG mud. 2500 lpm, 222bars, 120 rpm, 8kNm." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2760m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Flow check well. Pumped 5m³, 1.60sg slug, chased with 3.6m³ OBM." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2617m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH from 2760m to 2617m. Elevators not opening." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2617m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Trouble shooted problem with elevators and change out same." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2011m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued POOH from 2617m to 2011m. Pulling speed 1212 m/hours." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2011m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Changed out inserts in PS21's to 5''. Broke out X-over. Changed inserts in elevators to 5''." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1890m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Continued POOH from 2011m to 1890m. Pulling speed 484 m/hours. Elevators not opening." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1890m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Trouble shooted problem with elevators and change out same." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1035m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Continued POOH from 1890m to 1035m. Pulling speed 570 m/hours. Elevators not opening." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1035m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Trouble shooted elevator hydraulic problem." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 301m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Continued POOH with 5' DP from 1035m to 301m. Pulling speed 420 m/hours." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 301m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Changed handling gear to 3½'. Removed redundant hydraulic pressure gauges from elevators. PDM not able to turn." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 301m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Changed out sheared pin on PDM." "On 2009-01-10, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Hold tool box talk and POOH and lay out 3½' DP from 301m to 250m. Pulling speed 51 m/hours." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: Continued POOH and lay out 3½' DP from 250 to surface. Pulling speed 143 m/hours." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Prepared to pick up BHA - removed auto slips, installed masters and bowls, dressed elevators, turned PDM and changed roughneck dies." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Due to wind at 50 knots + no crane operation. Evaluated picking up BHA with PDM - no go due to lengths and components of tubulars." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on weather. Wind 50 kts plus. Performed general maintenance." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.5 hours. Operational details: WOW. Wind to high for deck crane to operate. Meanwhile prepared alternative solution to transport BHA to drill floor without using the deck crane. Wind 40-50 knots. Performed PM and house keeping." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: Held tool box talk regarding alternative option of picking up the BHA from cantilever with the PDM. Prepared paper work and equipment for picking up the BHA with the PDM." "On 2009-01-11, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 43m. The activity was categorized as 'plug abandon -- trip' and lasted for 7.2 hours. Operational details: Held tool box talk and picked up and made up 8½' BHA from cantilever. RIH from surface to 43m." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 100m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: Continued making up 8½' BHA. RIH from 43m to 100m. Inserted the radio active source." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 100m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Installed auto slips and function test same." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 588m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH with 8½' BHA on 5' DP from 100m to 588m. Tripping speed 650 m/hours. Extra time taken to pick/engage the 5' DP from the derrick due to high winds causing the 5' to rattling in the derrick." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 588m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Installed X/O on string and made up to TDS. Broke circulation and pumped 1300 lpm / 43 bar. Performed shallow test of Schlumberger tools. Ok." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1198m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Continued RIH with 8½' BHA on 5' DP from 588m to 1198m. Tripping speed 813 m/hours. Extra time taken to pick/engage the 5' DP from the derrick due to high winds causing the 5' to rattling in the derrick." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 1198m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Changed to 5½' handling equipment. Made up to TDS and filled the pipe." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 2560m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: Continued RIH with 8½' BHA on 5½' DP from 1198m to 2560m. Tripping speed 454 m/hours. Filled the pipe every 600m." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3072m. The activity was categorized as 'plug abandon -- trip' and lasted for 8.2 hours. Operational details: Washed down from 2560m to 3072m Tagged hard cement at 3072m set down 4 MT. Parameters: Flow 1400-1500 lpm at 60 rpm. Obstruction from 2835m to 2944m, took weight up to 5 MT. Worked down with various rates from 300 to 1760 lpm." "On 2009-01-12, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3090m. The activity was categorized as 'plug abandon -- trip' and lasted for 6.8 hours. Operational details: Drilled and attempted to kick off cement from 3072m to 3090m. Parameters: Flow 2140 lpm / SPP 145 bars / String RPM 130 TQ 13 kNm / WOB 2-3 / ECD 1.38 EMW / MUD weight 1.34 SG / ROP 1,5 mph. Up weight 155 MT / Down weight 140 MT / Free rotational weight 149 MT. Cement in returns 60 - 70%." "On 2009-01-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3095m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: Continued drilling and attempted to kick off from 3090m to 3095m. Parameters: Flow 2140 lpm / SPP 145 bars / String RPM 130 TQ 13 kNm / WOB 2-3 / ECD 1.39 EMW / MUD weight 1.34 SG / ROP 1-3 mph. Cement in returns 70 - 80%." "On 2009-01-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3141m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: Continued drilling and attempted to kick off from 3095m to 3141m. Increased parameters: Flow 2140 lpm / SPP 140-150 bars / String RPM 150 TQ 13-15 kNm / WOB 2-3 / ECD 1.39 EMW / MUD weight 1.34 SG / ROP 10-40 mph. Cement in returns 80%." "On 2009-01-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3141m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Continued drilling 8½' hole from 3141m to 3185m. Drilling parameters: Flow 2140 lpm / SPP 142 bars / String RPM 130 TQ 15-22 kNm / WOB 3-5 / ECD 1.4 EMW / MUD weight 1.34 SG / ROP 40 mph." "On 2009-01-13, at Well NO 15/9-F-15 A, a drilling event occurred at a depth of 3210m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.0 hours. Operational details: Kicked off at 3185m and drilled 8½' hole to 3210m 50/50 cement/formation. Drilling parameters: Flow 2140 lpm / SPP 144 bars / String RPM 130 TQ 12-26 kNm / WOB 2-5 / ECD 1.4 EMW / MUD weight 1.34 SG / ROP 4-6 mph." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 430m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Established circulation with 2800 lpm, 86 bar. Oriented tool face." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 459m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled/oriented 12 1/4' hole from 436 m to 459 m with 2800 lpm, 89 bar, WOB 3-5 ton. ROP 45-60 m/hr." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 500m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled/oriented 12 1/4' hole from 459 m to 500 m with 2800 lpm, 89-92 bar, WOB 4-7 ton. ROP 45 m/hr." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 500m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Removed cuttings blocking augers in lower shakers. Took survey. Reamed the interval from 485 m to 500 m with 3000 lpm, 100 bar, 38 rpm, 2-5 kNm." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 511m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled/oriented 12 1/4' hole from 500 m to 511 m with 3000 lpm, 100-105 bar, 38 rpm, 4-7 kNm, WOB 4-6 ton. ROP 45 m/hr." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 511m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Reamed the interval from 511 m to 473 m due to high dog leg. Reduced dog leg from 7 deg to 3 deg." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 511m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Removed cuttings blocking augers in lower shakers." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 553m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled/oriented 12 1/4' hole from 511 m to 553 m with 3000 lpm, 94-103 bar, 0-40 rpm, 3-5 kNm, WOB 4-6 ton. ROP 30-35 m/hr." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 553m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Reamed the interval from 553 m to 525 m to smoothen the well path." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 714m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled/oriented 12 1/4' hole from 553 m to 714 m with 3250-3500 lpm, 115-140 bar, 0-40 rpm, 4-8 kNm, WOB 4-8 ton. ROP 40-50 m/hr. Unable to receive GMWD survey." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 714m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Made several attempts to take GMWD survey without success." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 714m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Racked back stand. Took cluster shot survey." "On 2009-07-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 822m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled/oriented 12 1/4' hole from 714 m to 822 m with 3500 lpm, 140 bar, 0-40 rpm, 4-8 kNm, WOB 4-8 ton. ROP 30-40 m/hr." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 940m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled/oriented 12 1/4' hole from 822 m to 940 m with 3500 lpm, 147-155 bar, 0-40 rpm, 6-12 kNm, WOB 4-10 ton. ROP 30-45 m/hr." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 940m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Circulated hole clean prior to drill into Utsira formation. 3500 lpm, 150 bar, 40 rpm, 6-10 kNm." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 940m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated hole clean prior to drill into Utsira formation. 3500 lpm, 150 bar, 40 rpm, 6-10 kNm. Circulated totally 2 times BU." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 997m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled/oriented 12 1/4' hole from 940 m to 997 m with 3500 lpm, 147-155 bar, 0-40 rpm, 6-12 kNm, WOB 4-10 ton. ROP 30-40 m/hr. Top Utsira formation found at 959 m MD/882 m TVD." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 997m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Recorded parameters at TD: Up weight 124 tons, down weight 95 tons, rotation weight 109 ton with 20 rpm and 5-10 kNm." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 997m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pumped 6, 2 M3 of 1, 40 sg LCM pill. Displaced pill with 10 M3 1, 19 sg mud to spot LCM pill across the Utsira formation. 1300 lpm, 26-30 bar." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 915m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pulled out of hole from 997 to 915 m. Maximum over pull taken, 15 tons." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 915m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated the hole clean with 3800 lpm, 165 bar, 40 rpm, 6-14 kNm. Reciprocated the string while circulating. Circulated totally 4 times BU." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 915m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Displaced well to 1, 40 sg WBM. 3700 lpm, 155-170 bar, 40 rpm, 5-9 kNm." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 915m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Dropped a 3' drift into DP. Pumped drift down to dart sub. Pumped and displaced slug." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 395m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Pulled out of hole from 915 m to 395 m. Took maximum 15 ton over pull when pulling out from 915 m to 715 m. Slick hole seen above 715 m." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 395m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Recorded parameters above 13 3/8' casing window at 395 m: Up weight 107 tons, down weight 90 tons, rotation weight 99 ton with 20 rpm and 5-8 kNm." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pulled out of hole from 395 m to 230 m." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well on trip tank OK." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Performed safety check on TDS." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pulled out of hole from 230 m to 190 m." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pulled out of hole with 12 ¼' BHA from 190 m to 140 m." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Removed hydraulic power slips. Installed master bushing and bowls. Observed hydraulic leak on hydraulic elevator." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Repaired leak on hydraulic elevator." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Pulled out of hole with 12 ¼' BHA from 140 m to 80 m (LO dart sub and accelerator)." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Pulled out of hole and laid out 12 ¼' BHA from 80 m to surface." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned and tidied rig floor." "On 2009-07-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Rigged up 9 5/8' liner handling equipment on rig floor; held pre-job meeting with involved personnel prior to run 9 5/8' liner." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued to rig up 9 5/8' liner handling equipment on rig floor." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up 9 5/8' liner shoe and filled same with 1.40 sg mud and verified integrity of float - OK. Made up and ran in hole with 9 5/8' liner intermediate joint; tube-locked connection." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up and ran in hole with float collar joint; Filled liner with 1.40 sg mud and verified integrity of float - OK. Picked up and made up first standard 9 5/8' liner joint. Tube-locked connections." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 330m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Ran in hole with 9 5/8' liner from 40 m to 330 m. Filled every 3rd liner joint with 1, 40 sg mud." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 330m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Changed hose on hydraulic power slips." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 351m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Ran in hole with 9 5/8' liner from 330 m to 351 m. Filled every 3rd liner joint with 1.40 sg mud." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 351m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held pre job meeting with crew." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 375m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Ran in hole with 9 5/8' liner from 351 m to 375 m. Filled every 3rd liner joint with 1.40 sg mud. Unable to released draw work park bakes." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 375m. The activity was categorized as 'interruption -- maintain' and lasted for 2.2 hours. Operational details: Troubleshot joystick on drillers operating chair. Installed joystick from assistant drillers chair on drillers operating chair." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 423m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Ran in hole with 9 5/8' liner from 375 m to 423 Filled every 3rd liner joint with 1.40 sg mud." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 423m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up circulation swage and DP safety valve. Connected TDS. Circulated liner volume with 2000 lpm, 12 bars. BO circulation swedge and DP safety valve. Recorded weights prior to enter open hole: Up weight 94 tons, down weight 90 tons." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 424m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Ran in hole with 9 5/8' liner from 423 m to 424, 4 m. Took weight at 424, 4 m (Casing window). Maximum set down weight 17 tons. Made several attempts to pass through window with various orientations. BO last liner joint and installed same in hydraulic mouse hole. Installed circulation swage and DP safety valve. Stabbed liner joint and circulation assembly with PRS. Made up liner joint with casing tong. Connected TDS." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 435m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Established rotation with 5 rpm and 1-2 kNm. Ran liner through window with rotation from 424 m to 435 m. Broke out circulation swage." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 589m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Ran in hole with 9 5/8' liner from 435 m to 589 m. Filled every 3rd liner joint with 1,40 sg mud. Filled string. Confirmed remaining liner joints on deck-OK." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 589m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held pre job meeting prior to installing liner hanger." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 589m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed from 9 5/8' to 5 ½' handling equipment." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 598m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: P/U 9 5/8' liner hanger assembly from deck, made up MX ball seat/dual wiper plugs to running tool. Held pre-job safety meeting with involved personnel prior to operations. M/U and RIH with liner hanger assembly, set slips and filled liner PBR with drill water. Up/down weights = 117 / 99 tons." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 598m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged down casing tong." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with 9 5/8' liner on 5 ½' landing string from 598 m to 984 m; took 13 ton weight at 670 m, 722 m and 852 m. Washed down from 984 m to 997 m. Tagged bottom with 5 tons. Picked to up weight + 1 m." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Displaced well to 1, 20 sg WBM with 2090 lpm, 46 bars." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: M/U cementing head and connected surface line. Broke circulation with 500 lpm / 8 bar, washed down with 9 5/8' liner string from 994 - 997 m. Took up/down weights = 132 /107 tons. Positioned 9 5/8' liner shoe at 995 m." "On 2009-07-05, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Gradually increased pump rate to 2000 lpm / 45 bar, circulated open hole volume with 1.20 sg mud. Rotated the liner with 20 rpm and 10-19 kNm." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Reduced pump rate to 200 lpm / 8 bar, dropped setting ball and pumped same down pipe until landed out in ball seat. Set 9 3/8' liner hanger; pressured up to 165 bars for 2 min, than reduced pressure to 70 bars. Set down 25 tons and bled off pressure. Released liner hanger R/T according to Weatherford representative instructions; Pressured up on landing string to 240 bars, held pressure for 2 minutes and then bled off pressure. Pulled to up weight (97 tons) + 1 m to activate the MX ball seat. Set down 20 ton and sheared out ball seat." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Established circulation with 2000 lpm, 44 bar, verified stable returns. Reduced flow rate to 500 lpm, 10 bars and established rotation with 20 rpm, 10-19 kNm, Initial torque needed to establish rotation 39 kNm." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Circulated and conditioned mud prior to liner cementing job; broke circulation and gradually increased pump rate to 2000 lpm / 44 bar, circulated one open hole BU volume. Mud weights in/out = 1.20 sg, no losses seen. Meanwhile held pre-job cement meeting with involved personnel prior to liner cementing operations; reviewed check lists and relevant safety / operational issues. Leak tested surface cementing line to 300 bars for 10 min - OK." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped 20 m3 seawater followed by 20 M3 of 1, 35 sg spacer with rig pumps at 1550 lpm / 28-44 bars. Lined up to pump from cement unit, verified surface routing - OK." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released lower SSR dart. Mixed and pumped 13, 27 m3 1.92 sg cement slurry with cement unit at 700-900 lpm. Displaced surface cementing lines with 0.89 m3 fresh water. Released top dart. Lined up to pump seawater with rig pumps. Sheared out bottom SSR plug after 2, 9 M3." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced cement slurry in place with rig pumps: Started to pump at 800 lpm / 4 bars, observed bottom wiper plug shear. Increased pump rate to 2100 lpm / 21 - 80 bar, reduced to 600 lpm / 39 bar prior to bumping top plug. Bumped top wiper plug at 1074 strokes, corresponding to 97 % pump efficiency. No losses seen during the entire cementing and displacement operations." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Leak tested 9 5/8' liner to 70 bar above final circulation pressure for 10 min - OK. (Observed a small visual leak on cement head swivel). Bled off pressure and verified float - OK." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Set 9 5/8' TSP liner packer according to Weatherford representative instructions. Set down 28 ton and observed shear at 14 and 21 tons." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 400m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pulled liner hanger R/T out of liner hanger assembly; applied 50 bar pressure on pipe prior to operation, confirmed pressure drop. Circulated with 500 lpm, 6 bar while pulling out of PBR." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 400m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held pre job meeting. Laid out cement head with 1 single of DP below." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 400m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Installed 2 x sponge wiper balls in landing string. Circulated at 3100 lpm / 38 bar with sea water to clean out landing string and possible excess cement; no cement seen in returns." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 370m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pulled out of hole with landing string from 400 m to 370 m." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 370m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Water u-tube out of pipe. Connected TDS and continued circulating the hole clean with 3100 lpm, 40 bar." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pulled out of hole from 370 m to surface." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Removed hydraulic power slips. Broke out and laid out liner hanger running tool." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: While waiting on cement, cleaned and tidied rig floor. Aligned u-bolts on bails." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: While waiting on cement, BO and LD 11 ea 8 1/4' drill collars, and jar." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: While waiting on cement, Changed handling equipment and BO and LD 3 ea 9 3/4' drill collars." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: While waiting on cement, Held pre job meeting. Changed to 6 3/4' handling equipment. Picked up and racked back 7 ea 6 3/4' drill collars, accelerator and jar." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Made up RTTS assembly and ran in hole with same to 219 m. Installed pump in sub assembly." "On 2009-07-06, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Waited on cement. Meanwhile performed maintenance and service on drilling and pipe handling equipment. Cleaned and prepared pits for packer fluid." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Waited on cement. Meanwhile performed maintenance and service on drilling and pipe handling equipment. Cleaned and prepared pits for packer fluid." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated with 400 lpm, 5 bar to clean RTTS setting area from 215 m to 220 m. Set RTTS at 219 m, installed cement hose. Pressure tested surface lines to 120 bars for 5 minutes." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pressure tested TSP liner packer and 9 5/8' liner to 90 bars for 10 minutes with sea water. Pumped 0.175 l and bled back same." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released RTTS, waited for 5 minutes for packer element to relax. LO pump in sub assembly." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pulled out of hole with RTTS from 219 m to surface." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed to 5' handling equipment. BO and LD RTTS." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleaned and tidied rig floor. Held pre job meeting prior to PU 8 ½' BHA." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: Made up and ran in hole with 8 ½' BHA to 180 m." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 205m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Changed from 5' to 5 ½' handling equipment. Picked up 1 single DP from deck and ran in hole to 205 m." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 921m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Ran in hole with 8 ½' BHA on 5 ½' DP from 205 m to 921 m." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 967m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Filled pipe and established circulation with 1600 lpm, 54 bar, 30 rpm, 8 kNm. Washed down from 921 m to 967 m. Tagged top of float (Wiper plugs) at 967 m with 2 tons." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 996m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Drilled out wiper plug, casing FC, shoe track and 9 5/8' casing shoe from 967 m to 996 m with 1600 lpm, 55 bar, WOB 2 - 5 tons, 30 rpm, 8 - 13 kNm. Meanwhile held pre-job meeting with involved personnel prior to drill 8 ½' section; reviewed check lists and relevant safety / operational issues." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 997m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned out rat hole below casing shoe with 1600 lpm, 55 bar, WOB 0 - 1 tons, 30 rpm, 8 kNm. Simultaneously: Held pre job meeting prior to displace well from SW to 1.28 sg Soludrill mud." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 997m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Swept hole with 20 M3 hi-vis pill; 1600 lpm, 45 bar, 30 rpm, 8-9 kNm." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 997m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Pumped 20 M3 of spacer, Displaced well to 1.26 sg Soludrill mud, with 1600 lpm, 40-63 bar, 30 rpm, 8 kNm. Circulated 1 times BU after well displaced to condition mud." "On 2009-07-07, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1051m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled/oriented 8 1/2' hole from 997 m to 1051 m with 1600-1900 lpm, 80-105 bar, 30-60 rpm, 7-10 kNm, WOB 5-8 ton. ROP 45-50 m/hr. ECD 1.39-1.41 sg." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1206m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled/oriented 8 1/2' hole from 1051 m to 1206 m with 1900 lpm, 105-110 bar, 60 rpm, 8-10 kNm, WOB 5-9 ton. ROP 40-60 m/hr. ECD 1.41-1.43 sg." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1200m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Racked back stand. Attempted to take cluster shot survey, Observed torque peaks up to 19 kNm and 20 ton over pull when moving string after 2nd survey." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1200m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated the hole clean with 1930 lpm, 100 bar, 100 rpm, 8-9 kNm. ECD 1.42-1.40 sg." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1200m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated the hole clean with 1930 lpm, 100 bar, 100 rpm, 8-9 kNm. ECD 1.42-1.41 sg. Circulated totally 4 times BU." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1192m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Pulled out of hole from 1200 m to 1192 m. Attempted to take cluster shot survey; surveys out of specification. Took max 30 ton over pull when moving string. Pumped out of hole from 1192 m to 1158 m with 1700 lpm, 81 bar." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1192m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Attempted to take cluster shot survey, surveys still out of specification." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pulled out of hole from 1158 m to 1068 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Attempted to take cluster shot survey, surveys still out of specification." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 962m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pulled out of hole from 1068 m to 962 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 962m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well with bit inside 9 5/8' liner-OK." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 195m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Pulled out of hole from 962 m to 195 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 195m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well-OK." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pulled out of hole from 195 m to 140 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Removed hydraulic power slips and installed master bushing." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Pulled out of hole and racked back 8 ½' BHA from 140 m to 43 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: BO and LD 8 ½' BHA from 43 m to surface." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Cleaned and tidied rig floor." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held pre-job meeting with involved personnel prior to pick up and run in hole with cleanout assembly; reviewed check lists and relevant safety / operational issues." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 825m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.5 hours. Operational details: Made up and ran in hole with cleanout assembly to 825 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 945m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Ran in hole with cleanout assembly on 5 ½' DP from 825 m to 945 m. Broke circulation with 664 lpm, 8 bar. Up weight 102 tons and down weight 90 tons." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1202m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Ran in hole with cleanout assembly on 5 ½' DP from 945 m to 1202 m. Simultaneously: Held pre-job meeting with involved personnel prior to displace and clean well; reviewed check lists and relevant safety / operational issues." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up kelly cock and air operated ball release sub. Positioned mule shoe at 1205 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Established circulation and circulated 2 times bottoms up with 2000 lpm, 42 bar, 40 rpm, 4-6 kNm. Reciprocated string and scraped screen hanger setting area from 955 m to 946 m." "On 2009-07-08, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Displaced 1.26 sg Soludrill mud from open hole and up in 9 5/8' casing (1205 m to 746 m) by pumping 25 M3 of 1.20 NaCl brine with 2000 lpm, 40 bar." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Dropped 13/4' SABS opening ball. Displaced ball down with 400 lpm, 10 bar. Observed 55 bar pressure increase when ball sheared out ball seat." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued displacing well from 1.26 sg Soludrill to 1.20 sg NaCl brine. 3000 lpm, 38 bar, 40 rpm, 6 kNm." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Swept well with 15 m3 soap pill, 5 M3 1.20 sg brine and 15 M3 soap pill. 2000 lpm, 20-24 bar, 20 rpm, 6 kNm. Continued pumping 1.20 sg NaCl until clean brine in return and NTU readings below 200." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Emptied and cleaned trip tank. Filled trip tank with clean 1.20 sg brine." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flow checked well on trip tank. Gained 0.1 M3 the first 15 minutes due to thermal expansion, then the well was static." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1205m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Recorded parameters: Up weight 111 tons, down weight 94 tons, free rotation weight 103 tons, stretch 0.18 m and free rotation torque 5-7 kNm. BO kelly cock and air operated ball release sub." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 817m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pulled out of hole with cleanout assembly from 1205 m to 817 m. Recorded parameters at 951 m (screen hanger setting depth): Up weight 105 tons, down weight 91 tons, free rotation weight 98 tons, stretch 0.12 m and free rotation torque 4-5.5 kNm." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 817m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Held pre job meeting. Laid out cleanout assembly #3." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 743m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pulled out of hole from 817 m to 743 m." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 266m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Pulled out of hole from 743 m to 266 m." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 247m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pulled out of hole and laid out cleanout assembly #1 and #2 from 266 m to 247 m." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pulled out of hole from 247 m to surface. BO and LD mule shoe." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cleaned and tidied rig floor." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Held pre job meeting prior to rig up screen handling equipment." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 2.0 hours. Operational details: Rigged up screen handling equipment." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Held pre job meeting prior to run 6 5/8' sand screen." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 199m. The activity was categorized as 'completion -- sand control' and lasted for 4.0 hours. Operational details: Picked up, made up and ran in hole with 6 5/8' screens to 199 m." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 247m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: Made up XO and ran in hole with blank 6 5/8' liner from 199 m to 247 m." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 247m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Held pre job meeting prior to pick up liner hanger. Changed handling equipment." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 263m. The activity was categorized as 'completion -- sand control' and lasted for 1.2 hours. Operational details: Picked up made up and ran in hole with liner hanger assembly to 263 m. Filled PBR with drill water." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 263m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: Rigged down casing tong and installed hydraulic power slips." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1204m. The activity was categorized as 'completion -- sand control' and lasted for 2.8 hours. Operational details: Ran in hole with 6 5/8' liner screens on 5 ½' DP from 263 m to 1204.5 m. Tagged bottom with 5 tons." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1201m. The activity was categorized as 'completion -- sand control' and lasted for 0.8 hours. Operational details: Positioned string at 1201 m. Dropped 1 3/4' liner hanger setting ball and chased ball with 450 lpm, 8 bar. Pressure increased to 150 bar when ball landed in ball seat. Observed shear at 150 bars. Attempted to increase pressure to 165 bars, but pressure stabilized at 150 bars when pumping with 440 lpm." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1201m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Set down 30 tons to verify hanger set-OK." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1201m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: Adjusted down weight on hanger to 10 tons. Released running tool with 8 right hand turns. Attempted to pick up 1 meter but took full string weight. Pressured up to 165 bar and held pressure for 2 minutes. Set down 30 ton on hanger. Adjusted down weight on hanger to 10 tons. Bleed down pressure on string from 165 bars to 9 bars. Released running tool with 8 right hand turns. Pulled 1 m up and confirmed running tool free. Pressured up to shear out ball seat, ball seat sheared out at 255 bars." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 935m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Picked up 3.8 m to extend packer actuator dogs above the PBR. Sat down 30 ton on PBR to set liner hanger packer, observed booth 2 shears. Pulled running tool out of PBR." "On 2009-07-09, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 935m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: Prepared pit space and started mixing of 1.03 sg NaCl brine. Not done earlier due to pit capacity." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 935m. The activity was categorized as 'completion -- sand control' and lasted for 2.0 hours. Operational details: Continued mixing 1.03 sg NaCl brine. Meanwhile performed general rig maintenance." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 935m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: Displaced 9 5/8' and 13 3/8' casing to 1.03 sg NaCl with 3000 lpm, 63 bars." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 15m. The activity was categorized as 'completion -- sand control' and lasted for 2.8 hours. Operational details: Pulled out of hole from 935 m to 15 m. Tripped with reduced speed due to high friction in the well causing vibration in derrick." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 15m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: Removed hydraulic power slips and installed master bushing. Racked back stand." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: BO and LD liner hanger running tool." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: BO and LD liner hanger running tool." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Changed dies in iron roughneck. Cleaned and tidied rig floor." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Held pre job meeting prior to pick up swab cup assembly. Changed inserts in slips and elevator." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 267m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Picked up swab assemblies and ran in hole to 267 m." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 267m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed handling equipment. Meanwhile changed fitting on iron roughneck." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1187m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.8 hours. Operational details: Ran in hole with swab cup assembly on 5 ½' DP from 267 m to 1187 m." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1187m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated 1 time BU with 1500 lpm, 35-30 m." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1187m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 9.6 m³ of citric acid, 1.06 sg, displaced with 12.6 m³ 1.03 sg brine at 1500 lpm, 27 bars." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1187m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Observed well on trip tank. Gained 0.36 M3/hr for the first half hour due to thermal expansion, then levelled of and stabilized." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1120m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 11 times with 30 m strokes (1153-1123 m) 30 m/min. Ran back to 1187 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Pulled out of hole until upper swab cups above screens." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1120m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Monitored well on trip tank for losses. Loss rate 1.5 - 2 M3/min." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1120m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Stopped filling the hole from trip tank and let fluid level in annulus drop to equilibrium." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1187m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Ran in hole to 1159 m. Removed hydraulic power slips and installed master bushing. Ran in hole from 1159 m to 1187 m." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1187m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 6.2 m³ of citric acid, 1.06 sg, displaced with 12.8 m³ 1.03 sg brine at 1500 lpm, 29 bars. No return seen." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1170m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Laid out double DP, installed side entry sub and Kelly cock on string." "On 2009-07-10, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1170m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: Held pre job meeting. Performed cut and slip of drill line. Broke bolts on dead mans anchor gear box." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1170m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: Changed out broken bolts in gearbox on dead mans anchor." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1170m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Continued cut and slip operation. Found lock pin on dead mans anchor to be broken." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1170m. The activity was categorized as 'interruption -- maintain' and lasted for 1.8 hours. Operational details: Repaired lock pin on dead mans anchor." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1170m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Reset and tested anti collision system." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1153m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: BO side entry sub and Kelly cock. Installed double DP. Placed upper cup into the blank pipe." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1153m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pumped/bull-headed 30 M3 of 1.03 sg NaCl brine. 400 lpm, 4 bar. Increased flow rate to 1490 lpm, 28 bars after 15 M3 pumped." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 985m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Located lower swab cup inside the blank pipe and pumped/bull-headed 20 M3 of 1.03 sg NaCl packer fluid. 1500 lpm, 22 bar." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 930m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pulled out of hole from 985 m to 930 m. (Bull nose above the screen hanger)." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 930m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Mixed 90 M3 of 1.03 sg packer fluid. Not done earlier due to pit capacity." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 930m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Filled annulus with 85 M3 1.03 sg packer fluid. Loss rate decreased from 2 M3/min to 40 l/min after having displaced in 85 M3 of completion fluid." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 930m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Discussed further operation, could not find any surface reason causing the sudden decrease in loss rate. Decided to re-swab the well." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 995m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Ran in hole from 930 m to 995 m. Filled pipe and observed communication to trip tank, indicating flow past upper cup in blank pipe." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 930m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Swabbed the well 10 times with 30 m strokes (991-961 m) 30 m/min. Pulled out of hole to 930 m. (Bull nose above the screen hanger). Loss rate 1.2 M3/min. Stopped filling the hole from trip tank and let fluid level in annulus drop to equilibrium." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 270m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled out of hole from 930 m to 270 m. Filled hole with 2 M3/10 stand pulled." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 270m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed inserts in hydraulic power slips. Discovered that eye for safety wire on elevator inserts was damaged." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 270m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Welded on new eye for safety wire on elevator insert. Meanwhile greased dolly." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 270m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Was not able to rack back 3 1/5' DP in fingerboard. Initialized system-OK." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Continued pulling out of hole and lay out swab cup assemblies from 270 m to surface." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cleaned and tidied rig floor. Changed inserts in elevator." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up wear bushing running tool. Removed master bushing." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ran in hole. Engaged to wear bushing. Pulled out of hole with wear bushing. LO wear bushing and wear bushing running tool." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Made up riser/wellhead wash tool. Ran in hole and washed wellhead area with 1500 lpm, 5 bars. Past wellhead area 3 times. Pulled out and BO wellhead wash tool." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Made up and racked back tubing hanger assembly." "On 2009-07-11, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Held pre job meeting prior to RU for running ESP. Rigged up and spot equipment." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Rigged up and spot ESP equipment." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 14m. The activity was categorized as 'completion -- completion string' and lasted for 4.8 hours. Operational details: Picked up and made up ESP assembly 1 and 2. Connected control lines to motor. Made up ¼' hydraulic line from Multisensor gauge. Pumped oil into the motor by a hand pump. Serviced the motor and evacuated the air. Connected up the electrical cable to the motor and tested out same. Installed protectolizer clamp on the base of the motor." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 14m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Picked up and made up ESP assembly 3(ESP pump)." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Continued to make up ESP pump to protector. Installed clamp on ESP pump." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 18m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Picked up and made up ESP assembly 4(ESP discharge pressure assembly)." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 18m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held pre job meeting." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Picked up and made up bolt-on discharge head XO joint." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 33m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Picked up and made up first 7 5/8' tubing joint. Adjusted and aligned casing tong. Held pre job meeting prior to install hydraulic power slips. Installed clamp on tubing for protection while installing hydraulic power slips. Installed hydraulic power slips. Removed clamp." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 93m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Ran 7 5/8' tubing from 33 m to 93 m." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 81m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: LO 3 joints of tubing due to bad connections." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 105m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Ran 7 5/8' tubing from 81 m to 105 m." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 105m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: LO 1 joint of tubing due to bad connection." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 105m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Ran 7 5/8' tubing from 105 m to 117 m. LO 2 joints of tubing due to bad connections." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 105m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Discussed further operation. Decided to clean all pins and boxes, check threads and re-dope the tubing." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 176m. The activity was categorized as 'completion -- completion string' and lasted for 3.2 hours. Operational details: Ran 7 5/8' tubing from 105 m to 176 m." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 164m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: LO 2 joints of tubing due to bad connections." "On 2009-07-12, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 273m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: Ran 7 5/8' tubing from 164 m to 273 m." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 357m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Ran 7 5/8' tubing from 273 m to 357 m." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 357m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed electrical check of down hole system. Changed inserts in elevator. Confirmed remaining liner joints on deck-OK." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 357m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up tubing hanger/swivel assembly." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 357m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Broke FAST connection. Oriented the tubing hanger. Made up FAST connection. Cleared rig floor of redundant equipment." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 357m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed clamps on tubing for protection while removing hydraulic power slips and installing master bushing. Removed hydraulic power slips." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed penetrator incluning seals through hanger." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Schlumberger prepared for electrical cable splice." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 3.8 hours. Operational details: Spaced out and spliced cable." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Attached peneterator to hanger." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Pressure tested peneterator o-ring to 69 bar / 10 min. OK." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.2 hours. Operational details: Tested electric cable. TBT prior to pull mastrer bushing." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Ran hanger through rotary table. Had to remove master bushing." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH and landed hanger 20,92m in on landing string." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Checked electrical cable, OK." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Disconnected Tubing Hanger Running Tool and POOH with same." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: TBT prior to remove casing tong." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed casing tong." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: B/O and L/D Running Tool on deck." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared and cleaned rigfloor." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: TBT / SJA and preparation to pull diverter." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled master bushing, installed handrails around rotary. Installed lifting equipment for diverter." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: TBT prior to pull diverter." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled diverter and L/D same on deck." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged up double set of slings for pulling riser, held TBT." "On 2009-07-13, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Installed slings and attempted to pull riser. No go." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Continued attempts to pull riser. Moved riser, adjusted bolts, tried to re-position lock ring." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Could not disconnect riser from well head. Contacted town, trouble shot." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Troubleshot problems with lock ring between riser and wellhead. TBT with on comming crew." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: Adjusted release bolts to press lock ring in centre. Took 3 ton over pull, slacked off to neutral. Continued to adjust stroke of bolts. Riser free." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up riser, installed master bushing." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: TBT prior to L/D riser." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: L/D riser on deck." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Prepared wellhead for spacer spool." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Checked yellow tugger wire, OK. TBT prior to installation of spacer spool." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Installed flowhead and spacer spool according to Vetco procedures. Took 1 ton overpull verification test." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Removed and L/D lifting equipment. Cleaned rigfloor and wellhead area. Removed handrails on the weatherdeck." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.5 hours. Operational details: Leak tested cable peneterator seals in tubing bonnet to 69 bar / 10 min. OK. Meanwhile held TBT prior to disconnect Kelly hose." "On 2009-07-14, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.2 hours. Operational details: Leak tested bonnet cavity to 69 bar / 10 min. OK. Meanwhile started to disconnect kelly hose. END OF OPERATION F - 9A. WELL HANDED OVER TO PRODUCTION." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Well handed over from production. Held pre-job meeting for removal of flowline and ball valve. Lifted off F-9 hatch cover in moonpool." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Disconnected flowline from F-9. Secured same on XMT deck." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Prepared to remove ball valve from flow head assembly." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Prepared to pull diverter." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling diverter and securing same to DP in derrick." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed master bushings and outer ring, installed handrails around rotary. Installed diverter lifting eyes and connected lifting bridle." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled diverter and secured same to DP in derrick." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Performed TBT for removing ball valve from spacer spool and pulling spacer spool and tubing bonnet to drill floor." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Removed ball valve from spacer spool and secured same on XMT deck." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Rigged up to pull spacer spool and tubing bonnet to drill floor. Made up release bolts on tubing bonnet. Meanwhile Production dept shut-in nearby wells according to SimOps procedure." "On 2015-01-26, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Attempted to lift spacer spool and tubing bonnet without success, +/- 3 ton overpull. Slacked off weight and retried several times. No movement." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Reconfigured rig up and installed a 5 ton chain hoist for better control over weight taken. Simultaneously loosened ALT-2 release bolts. Attempted to lift tubing bonnet and spacer spool, 4 ton overpull, little movement observed, but still not free." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Removed chain hoist and re-attached double slings to ensure straight-up lift. Pulled up, backed out release bolts and pulled tubing bonnet free. Covered tubing hanger with bucket." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Lifted flow head assembly to drill floor, landed same on HTS. L/O assembly on deck. Meanwhile cleaned and greased wellhead." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for running riser" "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lifted riser to HTS. Installed shackles and slings for handling riser through rotary" "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Stop in operation due to call from Production dept regarding possible leak on well F-14. Waited until Production dept verified no leak." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lifted riser using TDS, tugger and crane. Tailed riser in to well center and disconnected crane and tugger." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran riser through rotary and landed off in WH. Took 8 ton overpull to confirm latch." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Build scaffholding in moonpool to remove handling slings from surface riser." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Disconnected and removed slings/shackles from riser and pulled same to rig floor. Removed slings from TDS chains." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: R/D scaffholding in moonpool. Meanwhile prepared for lifting diverter." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed TBT prior to attaching tension system to surface riser." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Installed tension system to riser in moonpool to allign riser with diverter. Meanwhile made canteliver ready for Schlumberger and planned for Schlumberger hang off point." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for installing diverter onto surface riser." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Ran diverter and landed off on surface riser. Installed overshot hose." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT for installing banana sheaves in derrick" "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 1.5 hours. Operational details: R/U sheave and slings in derrick for ESP cables." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: Moved Schlumberger equipment to drill floor." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 1.2 hours. Operational details: P/U diverter test tool and removed diverter bags." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Cleaned and tidied drill floor." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT prior to P/U tubing hanger running tool." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U TH RT. P/U and M/U 5 1/2' DP pup joint to same." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Problems with smart zone on drillfloor equipment. Stop in operation. Electrical technician investigated problems. Meanwhile performed TBT for running TH RT with new crew." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U 1ea 5 1/2' DP stand. RIH and landed out at 20.2 m." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Attempted to engage threads. Turned string 1/4 turn, string dropped 20 cm. Unable to turn string in any direction. Took 2 ton overpull." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Moved Weatherford casing handling equipment to drill floor. Meanwhile studied drawings and discovered that bullnose had landed outside of tubing hanger." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U, 3.5 ton hookload, and made TH RT free using link tilt on TDS. Pulled RT to surface for inspection. Observed some damage in rubber on bullnose. Tool ok to be re-run." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 386m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH and landed out at 20.8 m. Engaged threads and M/U RT to TH neck by rotating landing string 9 1/2 turns left with chain tongs, depth after M/U 20.9 m." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 368m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and pulled hanger free, 18.3t hookload. Pulled hanger up below rotary." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 358m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed master bushings and pulled TH through rotary. Checked 1st tubing joint for radioactivity, not radioactive." "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 358m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for L/D tubing hanger and R/U casing equipment" "On 2015-01-27, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 358m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: R/U casing handling equipment." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 358m. The activity was categorized as 'workover -- completion string' and lasted for 3.0 hours. Operational details: Continued installing casing handling equipment. Meanwhile checked banana sheave in derrick. Removed clamp from first tubing joint and cut ESP control cable." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 358m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for L/D hanger and POOH with 7 5/8' tubing." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 358m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: B/O tubing hanger assembly with RT. L/D and secured same on deck." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 358m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Changed BX inserts to 7 5/8' tubing. Moved AFT HRN back to allow more room for TDS to pass casing tong." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 297m. The activity was categorized as 'workover -- completion string' and lasted for 2.8 hours. Operational details: POOH with 7 5/8' tubing with ESP assemblies and control cable from 358 m to 297 m. Disconnected cable clamps and spooled power cable to the spooling unit." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 297m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Troubleshot and function tested guide arm on HTS. Meanwhile repaired Weatherford casing guide; removed guide arm, checked and secured piston." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 225m. The activity was categorized as 'workover -- completion string' and lasted for 2.8 hours. Operational details: POOH with 7 5/8' tubing with ESP assemblies and control cable from 297 m to 225 m. Disconnected cable clamps and spooled power cable to the spooling unit." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 225m. The activity was categorized as 'interruption -- wait' and lasted for 4.5 hours. Operational details: Secured drillfloor. Stop in operation due to crew change. Meanwhile observed missing armor on ESP cable pulled out of hole." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 225m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with new drilling crew for POOH." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 92m. The activity was categorized as 'workover -- completion string' and lasted for 3.2 hours. Operational details: POOH with 7 5/8' tubing with ESP assemblies and control cable from 225 m to 92 m. Disconnected cable clamps and spooled power cable to the spooling unit." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 92m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Performed TBT with new drilling crew for POOH." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: POOH with 7 5/8' tubing with ESP assemblies and control cable from 92 m to 21 m. Disconnected cable clamps and spooled power cable to the spooling unit. Recovered total 30 tubing clamps - none left in hole." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Performed TBT for changing handling equipment and L/D ESP assemblies." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Disconnected banana sheave from hang off line. Lowered sheave and cable to drill floor." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Removed Weatherford autoslips. Installed master bushings and Schlumberger stove table." "On 2015-01-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Commenced dismantling and L/D ESP assemblies." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 2.5 hours. Operational details: Pulled out and L/D ESP assemblies. Removed power cable and instrument line to multi sensor. Disconnected power cable from motor. Recovered 4 ea Protectorlisers and 1 ea special XO-clamp - none left in hole." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Removed casing tong to set back area. Cleaned and cleared rig floor." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: P/U recovered tubing hanger with RT from deck. B/O RT with chain tongs. Inspected seal areas on TH for damages - no damages observed. M/U RT to TH neck. L/D TH with RT to deck." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Performed TBT for wireline job. R/U WL equipment." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: M/U BHA for multifinger caliper log. Performed operational check of tool string." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 439m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: RIH with WL toolstring and corrolated tool at logging depth." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 18m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Opened caliper at 439 m and started logging up at 10 m/min." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 18m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Closed caliper at 18 m. Pulled cable head to surface and hung off in C-plate." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 18m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Waiting for approval of caliper log. Meanwhile performed TBT for R/D WL equipement." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: L/D WL toolstring and R/D WL equipment." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for installing bore protector." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed master bushings. M/U running tool and bore protector. RIH on 5 1/2' DP and installed boreprotector. POOH with running tool. R/B DP stand and installed master bushings." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for running Timelock plug." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: P/U Timelock plug, RIH with same on 5 1/2' DP to 45 m. Installed diverter inserts." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 369m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH w/Timelock plug on 5 7/8' DP from 45 m to 369 m. Avg. tripping speed 162 m/hr." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 369m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT for washing down and setting plug." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 395m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued RIH from 369 m to 395 m. Lined up to wash top of PBR, verified line up against closed IBOP. Bled off pressure." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 395m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Started to pump drill water at 300 lpm. Increased rate to 1100 lpm / 0 bar and washed top of PBR." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 395m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Attempted to set Timelock plug according to Archer procedures. Made 3 attempts without sucess. Archer rep contacted onshore support for advice. Performed TBT with new crew. Observed that the plug was not at the required setting depth - attempted set in 13 3/8' casing. RIH with Timelock plug from 395 m to 424 m." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 426m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Washed plug setting area and sat Timelock plug according to Archer instructions. Top of plug at 420,8 m. Positive indication of plug set. Closed ball valve and applied 30 bar to verify same closed. P/U and released running tool from plug." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up over shakers. Started pumping drill water from rig pumps. Increased pump rate to 2100 lpm / 0 bar and circulated 1 BU." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up cement unit to drillstring and performed line test against TDS IBOP to 100 bar. Bled back to 10 bar and opened TDS IBOP to confirm line-up." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed overboard valves. Lined up rig pumps and pumped drill water down string and up above diverter packer. Closed diverter packer. Line up to cement unit and attempted to pressure up well to 10 bar from cement unit. No success." "On 2015-01-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Checked line up and troubleshot loss of pressure." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Continued troubleshoot loss off pressure. Narrowed causes to a open needle valve on surface wellhead. Closed needle valve." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Lined rig pumps down string and pumped drill water to above diverter packer and closed same." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up cement unit to drill string. Pressured up well to 11 bar reference pressure. Pressured up to 34 bar using 101 litre. Pressure dropped and stabilized at 24 bar. Re-pressurized well to 34 bar using 34 litres 3 times while checking valves, diverter packer and well head for leaks. Pressure dropped and stabilized at 24 bar at every attempt." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 415m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Discussed situation with onshore duty. Meanwhile continued to check for possible leaking valves." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 442m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Opened diverter. Engaged and released Timelock plug." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 442m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with Timelock plug as drift using manual slips." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 935m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: RIH with Timelock plug from 442 m to 935 m to drift 9 5/8' liner." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 935m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed TBT with new crew for drifting 9 5/8' liner" "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 935m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Lined up manifold and shakers for washing down." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 940m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Started pumping drill water from rig pumps, 300 lpm. RIH to 938 m. Increased rate to 1100 lpm and washed from 938 m to 940 m." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 940m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to POOH." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 572m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: POOH with Timelock plug from 940 m to 572 m while filling pipe with trip tank pump. Pulled at restricted speed to prevent swabbing." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 572m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Lined up to perform line test from cement unit against IBOP. Tested same to 500psi, no good test. Troubleshot and re-tested line-up from cement unit. Not able to get good test through standpipe. Performed line test against valve K-1 on kill manifold, good test." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 572m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed TBT for setting Timelock plug. Recorded up/down weights prior to setting plug." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 602m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Sat Timelock plug at 600 m according to Archer procedures." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 595m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Closed ball valve and pressured up string to 35 bar to verify same closed. P/U and released RT from plug." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 595m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: R/U side-entry assy and TIW valve. Performed line test with cement unit. Test ok." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 595m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Filled well with drill water above diverter packer, closed same." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 595m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pressure tested casing with drill water from cement unit through side entry in drill string. Pressured up to 10 bar reference pressure using 190 ltr. Pressured up to 24 bar using 65 ltr and held pressure for 5 minutes. Pumped up to 28 bar using 16 ltr and held pressure for 5 min. Continued pressuring up to 32 bar using 16 ltr. Pressure broke off and dropped to 22 bar, pressure stable at 22 bar." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 595m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Evaluated situation." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 595m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Bled off 22 bar pressure on casing. R/D side entry assembly. Performed TBT with new crew." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 602m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Opened diverter packer. Engaged and released Timelock plug according to Archer procedures." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 425m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: POOH with Timelock plug from 602 m to 425 m while filling pipe with trip tank pump. Pulled at restricted speed to prevent swabbing." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 8m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: POOH with Timelock plug from 425 m to 8 m. Pulled at restricted speed to avoid swabbing." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: L/D primary Timelock plug and inspected same. No damages observed on packer elements." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 8m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: P/U backup Timelock plug." "On 2015-01-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 168m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: RIH Timelock plug on 5 1/2' DP from 8 m to 168 m. Avg. tripping speed 213 m/hr." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 409m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Continued RIH with Timelock plug on 5 1/2' DP from 168 m to 409 m. Avg. tripping speed 138 m/hr. Electrical Technician had to override/force singnal into control system to be able to operate PRS." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 436m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U TDS and washed down to setting depth, 300 lpm. Recorded up/down weights: 78 t / 86 ton and free rotational torque / weight at 10 rpm: 1000 Nm / 80 ton. Sat Timelock plug and closed ball valve according to Archer procedure. Pressured up string to 45 bar to verify ball valve closed. Packer mid element at 434,67 m." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 424m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: M/U side entry assy." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 424m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Filled well with water with rig pumps. Closed kelly cock, opened LTV and flushed lines from cement unit. Closed flowline valve and filled water above diverter packer element." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 424m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Performed line-up test from cement, 100 bar / 5 min. Verified" "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 424m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Attempted to pressure tested well to 34 bar against Timelock plug and diverter packer. Pressured up well in steps and monitored: 11 bar / 165 ltr 24 bar / 56 ltr 26 bar / 8 ltr 28 bar / 7 ltr 29 bar / 3 ltr 30 bar / 5 ltr (pressure drop observed) 31 bar / 9 ltr 32 bar / 8 ltr Aborted at 32 bar. Pressure dropped and stabilized at 23,5 bar. No good test. Bled off pressure to cement unit." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 424m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: R/D side entry assembly." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: POOH with Timelock RT on 5 1/2' DP from 424 m to 0 m. Avg. tripping speed 340 m/hr. L/D RT to deck." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: R/U for pulling diverter. Held TBT with new crew." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Installed lifting eyes and bridle. Pulled diverter inserts. 10' diverter inserts released from interlock, fell out and landed off on top of the riser." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Evaluated situation. Troubleshot to recover 10' inserts." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Planned and prepared retrieval tool to recover 10' inserts." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Tested retrieval tool. Good test." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Installed remaining retrieval tools and prepared for lifting 10' inserts." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Lifted 10' diverter inserts and recovered same to drill floor. Performed AAR with involved personnel" "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for pulling diverter." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Pulled diverter and R/B same." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Re-installed master bushings and removed tension lines from riser in moonpool." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.2 hours. Operational details: Build sacffolding in moonpool for installing shackles on riser. Meanwhile cleaned and cleared drill floor." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Installed lifting equipment onto riser. Removed scaffolding in moonpool. Drained the riser." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: R/U and prepared to disconnect and pull riser. Performed TBT for pulling riser. Meanwhile Production Dept shut-in adjacent wells according to SimOps procedure." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Nippled down riser and pulled same." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT with new crew for laying out riser joint." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: L/D surface riser on HTS with crane assist." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Retrived bore protector, utilising tuggers in TDS." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Lowered tubing bonnet to XMT deck utilising TDS. Landed tubing bonnet according to Vetco instructions. Production Dept. re-stared production according to SimOps procedure after tubing bonnet landed." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Blinded off cable penetrator. Installed flange on tubing bonnet. Lined-up cement unit to well by connecting 1/2' hose from moonpool manifold to WH." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Maersk and Halliburton cementer performed line walk to verify line-up. Performed TBT prior to pressure test casing." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Barried off moonpool and WH area. Filled up well from cement unit. Installed needle valve at WH." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Closed valve at WH and performed line-up test to 35 bar / 100 bar. Bled off pressure to cement unit after good test. Pressured up 10 bar, opened valve at WH and observed pressure drop." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Pressure tested well to 35 bar against Timelock plug and tubing bonnet. Pressured up well in steps and monitored: 10 bar / 11 ltr 28 bar / 33 ltr (observed instant pressure drop to 25,5 bar when stopping pumps) 30 bar / 4 ltr (instant drop to 27,4 bar) Continued pressuring up at lowest possible rate to reduce pressure drop when stopping pumps due to the 1/2' hose. 32 bar / 2 ltr (instant drop to 31,2 bar) 36 bar / 2 ltr (instant drop to 35,1 bar) Total 41 ltr pumped from 10 bar to 35,1 bar. Bled back same volume to cement unit after good test." "On 2015-01-31, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Disconnect bonnet and prepared to pull same. Performed TBT for pulling tubing bonnet and running surface riser. Removed master bushings. Meanwhile Production Dept shut-in adjacent wells according to SimOps procedure." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Released tubing bonnet from wellhead ustilising slings in TDS bails. Pulled tubing bonnet to drill floor." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U surface riser from HTS with assistance from crane. Tailed riser in to well centre. Lowered riser through rotary and landed off in WH. Took overpull to confirm latch. Production Dept re-started production from adjacenet wells according to SimOps procedure." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Disconnected slings from riser and R/U to lift diverter" "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Performed TBT for installing diverter. Lifted diverter from setback with TDS. Installed diverter in housing. Removed lifing eyes and slings from diverter. Energized diverter. Installed master bushings." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Removed chains from bails. Clean and cleared rig floor. Installed BX elevator." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Performed TBT for installing boreprotector. M/U RT to DP stand and attached boreprotector to same. RIH and installed boreprotector in WH. POOH with RT, B/O and L/D same." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 5m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for retrieving Timelock plug on 5 1/2' DP. P/U and M/U Timelock RRT." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 430m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: RIH with Timelock RRT on 5 1/2' DP from 5 m to 430 m. Avg. tripping speed 425 m/hr." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 430m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Engaged and released Timelock plug according to Archer procedures." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 241m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: POOH Timelock plug on 5 1/2' DP from 430 m to 241 m. Avg. tripping speed 189 m/hr." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 241m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT with new crew for POOH." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 8m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: POOH Timelock plug on 5 1/2' DP from 241 m to 8 m. Avg. tripping speed 186 m/hr." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: L/D Timelock plug and RRT on deck." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Lifted WL tools to drill floor and prepared same." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U and run WL" "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: R/U WL equipment and P/U ME-plug toolstring" "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Tested toolstring and zeroed depth in RKB." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1195m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: RIH with ME-plug. Lost weight at 952 m. P/U to 900 m, RIH at higher speed and passed obstruction. Continued RIH. Lost weight at 1163 m. P/U to 1130 m, RIH at higher speed and passed obstruction. Continued RIH and tagged TD at 1195 m." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 1190m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: P/U until tension in string. Activated setting tool and set plug according to Interwell procedure. Observed tension drop from 1320 lbs to 790 lbs, indication of plug set. RIH and tagged plug. Top plug at 1187,81 m. Mid element at 1188,87 m." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 8m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH with WL toolstring. Simultaneously performed TBT for R/D WL equipment." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: L/D WL toolstring and R/D wireline equipment." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for pulling boreprotector and installing casing tong." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Cleared set back area for Weatherford casing tong." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: P/U boreprotector RRT. RIH with same on DP to surface WH. Engaged boreprotector and pulled same to surface. L/D boreprotector RRT." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: R/U Weatherford casing tong." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT for R/U Schlumberger equipment and M/U ESP assemblies. Installed stovepipe above rotary." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: P/U ESP assembly 1 - Multisensor and motor. Landed lifting clamp on stovepipe in rotary. Serviced motor according to Schlumberger procedures." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 14m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Performed TBT with new crew. P/U and M/U ESP assembly 2 - Protector. RIH and landed off in stovepipe." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: P/U and M/U ESP assembly 3 - ESP pump. RIH and landed off in stovepipe." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: P/U and M/U Discharge pressure assembly (assy 4) to ESP pump." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Changed inserts in elevator to 7 5/8'. Installed rotating arm on elevator." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 17m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: P/U and M/U ESP assembly 5 - Bolt on discharge and XO." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Pulled back to Multisensor and connected hydraulic line to same. Pressure tested to 3000 psi / 15 min." "On 2015-02-01, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Pulled ESP electrical cable to rig floor. Feed cable through banana sheave and installed sheave to PRS." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Connected pothead to ESP motor" "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 14m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Serviced seal on protector and filled with oil." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Installed protectolizer clamps and terminated hydraulic lines. Secured string with manual slips." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT for running 7 5/8' tubing with cable." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: P/U first 7 5/8' tubing joint from HTS. Attempted to M/U same to ESP assy. Not able to get good connection. Trouble to B/O connection. B/O and observed damaged threads. L/O tubing joint." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Evaluated situation." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: B/O and L/D Bolt on Discharge assembly (ESP assy #5) due to damaged threads." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with new crew." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: P/U and M/U the Bolt on Discharge assembly (ESP assy #5) retrieved from F-9 A." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: P/U first 7 5/8' tubing joint from HTS. M/U same to ESP assy. Pulled up and installed clamps." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT for pulling master bushings and install spider slips." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Troubleshot fault on PRS." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Installed banana sheave onto hangoff wire." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Installed wire clamp. Pulled master bushings and installed spider slips on tugger." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 350m. The activity was categorized as 'completion -- completion string' and lasted for 7.2 hours. Operational details: RIH with ESP assemblies on 7 5/8' tubing from 21 m to 348 m. M/U control line clamp on every connection. Average 4,1 joints/hr. Schlumberger tested ESP and cable at 134 m, 212 m and 290 m." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 350m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT with new crew. Changed inserts in BX-elevator to 5 1/2'." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 350m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Changed to larger sized Weatherford tong." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 350m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U tubing hanger assembly from HTS. Tailed into well centre with crane assist. M/U tubing hanger to 7 5/8' tubing." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 360m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH with tubing hanger assembly. Check orientation of alignment key. Spaced out to break FAST connector with casing tong and set slips on tubing pup below FAST connector. Undid top flange on FAST swivel." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 360m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: B/O FAST connector with casing tong. Made several attempts. Had to change jaws and adjust rollers in tong. Adjusted casing tong torque and B/O at 20000-25000 ft-lbs." "On 2015-02-02, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 360m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Released and pulled up FAST sleeve. Oriented hanger according to Vetco instructions. Cleaned and doped threads." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 355m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U FAST sleeve to tubing hanger." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 355m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for removing compact spider." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 355m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed compact spider and parked same in set back." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 355m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH with tubing hanger to working hight. Mounted penetrator in TH, measured cable cutting point. Disassembled penetrator and spaced out for cable splice." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 355m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Electrically checked downhole system. Cut main cable and spooled back remaining ESP cable. Spliced cable to penetrator pigtails. Electrically checked system after splicing." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 355m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Performed TBT for RIH with tubing hanger" "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 355m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: R/D Weatherford casing tong and moved same to set back. Removed Weatherford 7 5/8' tong from drill floor." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 360m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH with TH. M/U power penetrator to hanger. Installed cable clamps and adjusted cable to take out slack in same." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 360m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Leak tested power penetrator to 69 bar / 10 min." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 366m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed master bushings and RIH with tubing hanger." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 366m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Troubleshot PRS. Repaired hydraulic fittings on forward PRS upper head." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 380m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Recorded up/down weight 86 ton / 82 ton. RIH and landed tubing hanger. Sat down 10 ton." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 380m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed electrical testing of ESP system through landing lead." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Disconnected tubing hanger RT. POOH and L/D same." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for pulling diverter." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed link adaptor and elevator. Installed chains and diverter bridle. Meanwhile bled down overshot." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared drill floor. Pulled master bushings and prepared to pull diverter." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Stopped operation on drill floor due to exhaust fumes. Production switched over to generators and turned off turbines." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled diverter and landed same off on set back." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and attached slings from riser to chains. Removed tarp and nylon covers in moonpool. Meanwhile Production Dept shut-in adjacent wells according to SimOps procedure." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for pulling riser." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Disconnected riser. Pulled same to surface and L/D on HTS." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Prepared for running tubing bonnet and spacer spool through rotary on TDS." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Performed TBT for lowering tubing bonnet." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Lowered tubing bonnet with spacer spool through rotary and installed same on surface well head. Production Dept informed when heavy lift landed." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.5 hours. Operational details: Leak tested penetrator seals in tubing bonnet to 69 bar / 10 min. Leak tested annulus insert valve to 69 bar / 10 min. Leak tested tubing bonnet cavety to 69 bar /10 min." "On 2015-02-03, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Installed ball valve. Commenced nippling up flowline." "On 2015-02-04, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 3.5 hours. Operational details: Continued nippling up flow line. Meanwhile installed hatches above F-9. ESP workover on F-9 A finalized. Commisioning to be performed offline." "On 2016-09-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.8 hours. Operational details: Performed preparations for skidding, disconnected injection and bleed off hose to allow skidding. Meanwhile deck crew worked on unloading cargo boat. Performed 3 monthly PM on TDS. Deck crew worked w/ helicopter 18:25" "On 2016-09-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.5 hours. Operational details: Continued to offload critical equipment from supply vessel. Meanwhile carried out maintenance on TDS and FWD PRS. Deck crew worked w/ helicopter 21:55" "On 2016-09-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to skid cantilever" "On 2016-09-28, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Removed stairs and bridge to Production module" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.2 hours. Operational details: Skidded cantilever to 1.5m port and 6.75m aft to F09" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to N/D spacer spool and tubing bonnet" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Prepared for lifting of spacer spool and tubing bonnet w/ ball valve, using double lift slings from top drive. Opened ball valve. Released lock ring on tubing bonnet. Lifted assembly trough rotary and L/D. Removed C-ring. Meanwhile built scaffolding around F09" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to run surface riser" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Connected lifting bridle to surface riser, attached crane for tailing riser in. P/U riser, RIH, connected same to wellhead. Secured riser in moonpool and removed lifting bridle" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to handle diverter" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U and run diverter, pressured up system. Installed outer rings, master bushing and BX elevators to bails" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to spot casing tong" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Spot casing tong and slips on rig floor. Meanwhile fill well with SW using trip tank, unable to keep well full" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U TH running tool, RIH same and engage to TH" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled TH with 20t overpull, POOH and racked DP stand" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U casing tong" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U casing tong on the rig floor" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Removed master bushing and pulled TH above RKB. L/D TH assembly to deck. Changed BX inserts and installed power slips" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Attempted to move TH to cantilever with PDM, too high winds" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to move TH from HTS to starboard side of the rig floor" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 346m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Moved TH from HTS and landed on starboard side of drill floor" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 212m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Pulled and L/D 7 5/8in tubing, spooled ESP cable at the same time. Average pulling speed 5,3joints/hour. Totally pulled 12 joints" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Accidently dropped 212m of tubing string by operator error. Performed time out for safety conversation with all involved. Took pictures" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: L/D tubing joint from HTS, removed power slips and R/D casing tong. Meanwhile inspected PRS before further use. Problem with FWD PRS. Moved casing tong to forward IRN track." "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: P/U and M/U spear BHA to fish 7 5/8in tubing string. RIF and tagged top of the fish at 200m" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 200m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Worked string f/ 200.1m to 200.7m with up to 6t WOB while rotating at 5rpm CCW 5kNM. Not able to engage the fish" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 8m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: POOH w/ spear BHA from 200m to surface. Inspected spear. Observed bull nose missing in the well" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation. Meanwhile performed TBT to pick up junk mill BHA" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 30m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U and M/U junk mill BHA" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 200m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: RIH w/ junk mill BHA to 194m. M/U TDS, took up/down weights 80t/76t. Tagged top of fish at 200m w/ 5t" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 200m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation. Agreed to carry on with setting EZSV and surface cement plug" "On 2016-09-29, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: POOH w/ junk mill BHA. L/D same" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to run 13 3/8in EZSV plug" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 55m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: P/U and M/U 13 3/8in EZSV plug to stand of drill pipe. RIH. M/U 2x 3m pups for space out" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 200m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ EZSV BHA on 5,5in DP. Tagged top of fish at 200m w/ 1t" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 200m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Established circulation and washed the setting area, 550 l/min/ 4 bar. Installed the 13 3/8 EZSV plug at 199,2 m top of plug (35 right hand turns). Load tested the plug with 10t down weight" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 196m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: L/D single, P/U and M/U pump in sub and TDS" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 196m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Circulated well to sea water at 3400 l/min - 11bar, 50 rpm until clean returns of below 30ppm OIW content. Totally circulated 20m3" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 199m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/U cement hose and confirmed line up" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 199m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Balanced cement plug (148 m - 199 m ): Mixed and pumped 5,0 m3 of 1,95 SG cement slurry, 600 l/min. Displaced the cement with 1800 l of drill water 1000 l/min/ 14 bar. Pulled out of cement to 148m at 2 min/stand. Theoretical TOC 148 m" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/D cement hose and pump in sub" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 148m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Installed pup with sponge ball. Staged up pumps to 3100 l/min - 18bar. Circulated 1,5BU. Diverted returns overboard. Observed cement in returns on shakers" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ EZSV running tool. L/D same" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Clean and cleared rig floor" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to handle diverter" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed BX elevators and connected chains to bails. Pulled master bushing and outer ring" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Connected lifting chains to diverter, pulled and secured same in setback area" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D surface riser" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Connected bridle to surface riser, pulled and L/D same" "On 2016-09-30, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed hatch covers for F09 in moonpool" "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Performed TBT for skidding to F-9 A and tag TOC" "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Skidded cantilever to well F-9 A" "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Performed TBT for removing hatches." "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Removed hatches. Installed masterbushing" "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: RIH on 5 1/2' DP open ended. Tagged TOC at 152 m." "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Performed TBT for manual handling" "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: POOH 5 1/2' DP to surface." "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Installed hatches and hole covers. Performed pre-skid checks" "On 2016-10-16, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.5 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Closed doors on BOP. Cleaned shaker pits. Cleaned out dry bulk silos" "On 2016-10-17, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather to pull production riser on F-15 D Meanwhile: Closed doors on BOP. Cleaned shaker pits. Cleaned out dry bulk silos **** END OF REPORT ****" "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding" "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded to STB. Lifted down deck covers from main deck to WH deck. Skidded AFT then PORT, to well center F-9 A." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed post-skid checks. Installed stairs to cantiliver." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Removed hatch and installed scaffolding in moonpool and WH deck." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U and M/U Cutter BHA and inner string. P/U and M/U spear assy. Engaged spear, took 20 ton overpull to confirm." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Load shifted weight from tension cylinders to TDS" "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D tension cylinders." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D boat collision stool and tension ring. Upper centralizer stuck, unable to remove. Installed diverter and hose on WH." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Staged up flow to 2400 lpm / 80 bar. Cut riser. Observed drop of overpull, good indication of cut." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew" "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D diverter and hose from WH. R/U chain hoist for pulling upper centralizer." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled riser. Removed upper centralizer (pulled free centralizer with riser flange when pulling the riser). Built scaffolding around hole openings. Installed wooden blocks to reduce riser movement." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with riser and landed onto C-plate on drill floor." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U false rotary POOH with inner string. R/B spear and cutter assy." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U spear assy and engaged in riser. R/D false rotary and C-plate. Removed BX-elevator and R/U manual elevator on riser. Landed riser on manual elevator. Lached bails onto manual elevator." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with riser (Lift #1). Cleaned off marine growth on centralizer deck. Meanwhile: Emptied pit 6 (clean SW)." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U cutting machine. Cut tensioner joint. Significant wave height 1,5 m. R/D cutting machine." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: L/O tensioner joint. Installed link tilt pins on elevator." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with riser (Lift #2). Cleaned off marine growth on centralizer deck." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine. Cut riser joint. Significant wave height 2,2 m. R/D cutting machine." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #2). POOH with riser (Lift #3). Cleaned off marine growth on centralizer deck." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine. Cut riser joint. Significant wave height 2,1 m. R/D cutting machine." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #3). POOH with riser (Lift #4). Cleaned off marine growth on centralizer deck. Riser out of splash zone at 16:30" "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine. Cut riser joint. R/D cutting machine." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #4). POOH with riser (Lift #5). Cleaned off marine growth on centralizer deck." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine. Cut riser joint. R/D cutting machine" "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (Lift #5). POOH with riser (Lift #6). Cleaned off marine growth on centralizer deck." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine. Cut riser joint. R/D cutting machine" "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O riser joint (Lift #6). POOH with riser (Lift #7). POOH and L/O stress joint." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Clean and cleared drill floor." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed saddle and riser bucket from HTS." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: L/O cutting - and spear assy." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installing hatches and hole covers." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Lifted tension cylinders from WH to drill floor." "On 2016-10-23, at Well NO 15/9-F-9 A, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed hatches. **** END OF REPORT ****" "On 2013-08-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2627m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued to kick off from F-1 A. Drilled 12 1/4' hole from 2617 m to 2627 m as per Baker DD instructions. WOB 2 - 5 tonne. 2800 l/min/ 153 bar. 40 rpm / 13 - 17 kNm. Started bleeding in LCM premix, 4m3 per stand for drilling Ty Fm." "On 2013-08-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2650m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 12 1/4' hole from 2627 m to 2650 m. Average ROP 11,5 m/hr. WOB 3 - 6 tonne. 3500 l/min/ 215 - 220 bar. 80 rpm / 15 -18 kNm. ECD 1,32 SG. Bleed in LCM premix as per plan to maintain particle concentration. Initially controlled ROP to 10 m/hr." "On 2013-08-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2763m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and oriented 12 1/4' hole from 2650 m to 2763 m. Average ROP: 22,6 m/hr, WOB 2 - 6 tonne. 3500 l/min/ 215 - 220 bar. 80 rpm / 17 - 21 kNm. ECD 1,32 SG. Bleed in LCM premix as per plan to maintain particle concentration." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2820m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled and oriented 12 1/4' hole from 2763 m to 2820 m. Average ROP: 21,6 m/hr WOB 3 - 11 tonne. 3500 l/min/ 217 - 230 bar. 100 rpm / 17 - 29 kNm. ECD 1,32 SG. Maintained LCM background concentration." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2820m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Cleared tripped cuttings conveyor." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2903m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled 12 1/4' hole from 2820 m to 2903 m. Average ROP: 19,5 m/hr. WOB 9 - 12 tonne. 3500 l/min / 220 - 235 bar. 100 rpm / 11 - 29 kNm. ECD 1,31 SG. Maintained LCM background concentration." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3010m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 12 1/4' hole from 2903 m to 3010 m, Average ROP: 21,4 m/hr, WOB 9 - 12 tonne. 3500 l/min/ 225 - 230 bar. 100 rpm / 20 - 30 kNm. ECD 1,31 SG. Maintained LCM background concentration." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3097m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled 12 1/4' hole from 3010 m to TD at 3097 m. Average ROP: 16,6 m/hr WOB 10 - 14 tonne. 3500 l/min/ 225 - 238 bar. 100 rpm / 20 - 25 kNm. ECD 1,31 SG. Section TD at 3097 m. Maintained LCM background concentration." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3097m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took TD survey and downlinked to ribs off." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3097m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated hole clean w/ 3500 l/min/ 212 - 220 bar, 100 RPM / 12 - 15 kNm, ECD 1,30 SG." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3071m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated hole clean w/ 3500 l/min/ 210 - 212 bar, ECD 1,30 SG. Circulated total 3 B/U, 690 m3. Racked one stand. Meanwhile repaired hydraulic leak on TDS allignment cylinder. Serviced TDS and dolly." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3071m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Well stable. Meanwhile performed TBT for drop down Gyro." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3071m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Dropped gyro." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3096m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH to bottom." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2900m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH w/ 12 1/4' BHA and drop gyro on 5 1/2' DP from 3096 m to 2900 m. Pulled 5 stands wet." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2900m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pumped 4m3 slug and chased same. Filled trip tank." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2864m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Continued to POOH with 12 1/4' BHA and drop gyro on 5 1/2' DP. Baker mud logging unit shut down due to high winds." "On 2013-08-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2864m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Troubleshoot logging unit and prepared temporary wind protection on air intake." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2700m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: POOH w/ 12 1/4' BHA. Controlled speed while monitoring volumes with rig sensors. Meanwhile arranged wind protection and re-booted logging unit." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH w/ 12 1/4' BHA and drop gyro into the casing shoe." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Well stable." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 448m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH w/ 12 1/4' BHA on 5 1/2' DP from 2590 m to 448 m . Avg. tripping speed 856 m/hr." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 448m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Took rotational shot surveys as per Scientific instructions." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' BHA from 448 m to 247 m." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min prior to pull BHA through BOP. Well stable. Hold TBT for handling BHA." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH 12 1/4' BHA on HWDP. Racked HWDP stands." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Recovered gyro tool string and L/D same." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed PS21 slips and installed master bushings." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: L/D 12 1/4' BHA from 125 m to 32 m as per Baker DD lay down plan." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Plugged into OnTrak and downloaded data." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: POOH to 3 m, plugged into CoPilot and downloaded data." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Cleaned and layed out BHA, inspected bit. Bit grading: 0-2-WT-T-X-1/16-NO-TD." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up bullnose jetting sub and WBRRT." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH to 138 m, restricted speed due to fullbore tool. M/U TDS and jetted well head area with 1500 lpm, 15 bar." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 181m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH from 138 m to 181 m, set down 5 tons and checked measurement for casing hanger run. Pulled WB with 37 tons overpull." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH from 181 m to 138 m, jetted wellhead area with 1500 lpm, 15 bar. Dropped drift and POOH to surface. L/D WB, reset tool and L/D same." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleaned and cleared rigfloor." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Moved Weatherford tong into position, arranged hoses and JAM unit." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Hold TBT prior to slip and cut operation." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Rigged up, slipped and cut 44 m drill line. Cleaned and cleared rig floor." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Calibrated blocks with both rig and Baker systems." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Tidied rigfloor prior to rigging up casing equipment." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: R/U handling equipment for 9 5/8' casing. Changed bails and installed elevators, function tested same. Removed bushings and installed FMS. Function tested same." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to pick up shoe joint." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U 9 5/8' shoe joint from deck, checked float ok." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Installed Weatherford fill-up tool. Installed bypass baffle." "On 2013-08-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: M/U shoe joint to float collar/intermediate stand from derrick. Thread locked connection." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH shoetrack, P/U single joint from deck and M/U same." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 209m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 9 5/8' 53,5ppf P110 Vam TOP casing from 63 m to 209 m . Run casing in stands from derrick. Filled every stand." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 209m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed leaking mud saver valve." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1207m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: RIH with 9 5/8' 53,5 ppf P110 Vam TOP casing from 209 m to 1207 m. Run stands from derrick. Filled casing every stand. Average running rate 5,5 stands/hr" "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2489m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: RIH with 9 5/8' 53,5ppf P110 Vam TOP casing from 1207 m to 2489 m. Run stands from derrick. Filled casing every stand. Average running rate 7,1 stands/hr." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2489m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed to 10 3/4' elevators and tong jaws." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2489m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U x-over joint from deck and M/U same." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2489m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Changed out slips to 10 3/4' and changed die blocks in casing tong." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2944m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with 10 3/4' 65,7ppf P110 Vam TOP casing from 2489 m to 2944 m. Run stands from derrick. Filled casing every stand. Average running rate 5 stands/hr." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2944m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT before rigging down casing running equipment." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2944m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: R/D casing fill-up tool, bails, elevator and rotator. Installed bails and elevators for 5 1/2' DP." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2944m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed TBT before picking up casing hanger." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2944m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U, cleaned and M/U casing hanger." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2944m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed PS30 slips and installed outer ring and master bushings. RIH hanger below rotary." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2954m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: R/D handling equipment for 10 3/4' casing, R/D casing tongs and cleared rig floor." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2994m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 9 5/8' x 10 3/4' casing on 5 1/2 HWDP landing string from 2954 m to 2994 m. Circulated string with 500 lpm while RIH." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3089m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH on landing string from 2994 m to 3089 m. Circulated string with 500 lpm while RIH." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3089m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out HWDP double from LS." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: P/U cement stand. M/U cement hoses and control lines. M/U cement stand to landing string. Landed casing hanger in wellhead as per Vetco instructions. Confirmed hanger set as per procedure." "On 2013-09-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Increased flow in 250 l/min steps to 2500 l/min/ 80 bar. Let flow and pressure stabilize on each step. No losses to formation." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated prior to cement job 2500 l/min 80 - 85 bar. After 1,15 x B/U experienced a 5 bar pressure drop and indication of losses. Checked surface equipment, ok." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Established loss free rate at 1350 lpm/ 45 bar. Lost 3,2 m3 of mud in total during circulation. Held TBT prior to cement job." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Pumped 22 m3 of 1,60 SG spacer with rig pumps, pumped with loss free rate 1350 lpm. Lined up from cement unit and verified line-up. Released dart for bottom plug, verified flag indication. Mixed and pumped 14 m3 1,90 SG slurry at 680 lpm, Released top dart and observed top plug release at 950 l pumped and 82 bar. Chased cement w/ rigpumps and 2500 lpm. Displaced cement with 1300 - 1600 lpm. Used bottom plug landing shear to calibrate pump efficieny: 95,6% Displaced cement into annulus with 2000 lpm, following pump plan. Bumped top plug at 5190 strokes (95,6% efficency). Pressured up to 70 bar above final circulation pressure of 55 bar. Checked for back flow, floats holding. Lost in total 8 m3 OBM to formation." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Bleed off pressure and checked for back flow, floats holding." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Flushed manifolds after cement job and prepared for setting seal assembly." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Attempted to set seal assembly as per Vetco procedure." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Leak on Halliburton cement unit, trouble shoot and repaired same." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Set seal assembly as per Vetco procedure. Took 45 ton overpull, closed annular preventer and confirmed seal assembly set. Tested annular BOP against seal assembly 20/345 bar 5/10 min." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.2 hours. Operational details: Tested BOP pipe rams to 20 bar/ 5 min and 345 bar/ 10 min as per Maersk procedure." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Opened BOP, released PADPRT according to Vetco procedure." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: L/D cement head. M/U double to landing string. Installed sponge balls and circulated w/ 3500 l/min/ 37 bar." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH from 139 m to surface, cleaned PADPRT and checked lead impression blocks. L/O tool to cantilever." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: M/U bullnose, WBRRT and wearbushing. RIH to 139 m and landed WB, took 5 ton overpull." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Lined up and tested middle pipe ram to 20 bar/ 5 min and 345 bar/ 10 min." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Released WBRRT with 5 right hand turns, POOH to surface. Cleaned and reset running tool, L/O same." "On 2013-09-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleaned and cleared rigfloor. Continue reporting on F-99 during Maersk rig maintenance/rig survey." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: ***Report continuing from well 15/9-F-99, report #229*** Performed prejob meeting prior to pick up and make up 8 1/2' bottom hole assembly." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Picked up and made up 8 1/2' bottom hole assembly to 47m MD." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Uploaded and iniated Testrak and ontrak/copilot." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Picked up float sub and stabilizer. Washed and cleaned all ports." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Installed radioactive sources." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 198m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Picked up and made up 8 1/2' bottom hole assembly from 50m to 198m." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 198m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 198m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 198m to 1005m. Average tripping speed: 530 m/hr." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1005m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Filled pipe. Performed shallow test of MWD tools." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2013m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 1005m to 2013m. Average tripping speed: 672 m/hr." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2013m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Filled drillpipe." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2981m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 2013m to 2981m. Average tripping speed: 645 m/hr." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2981m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Performed choke drill." "On 2013-09-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3027m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Established circulation with 1500 lpm, 121 bar and 30 rpm. Washed in hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 2981m to 3027m." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3044m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Washed in hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe with 1500 lpm and 30 rpm from 3027m MD to 3044m MD. Tagged top of cement at 3044m MD with 5MT." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Established parameters at 2000 lpm, 192-200 bar and 60 rpm. Drilled through top wiper plug from 3044m MD to 3047m MD. Meanwhile: Increased mud weight from 1.28 sg to 1.32 sg." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled shoetrack and shoe from 3047m MD to 3090m MD with 2000-2200 lpm, 198-206 bar, 60-80 rpm, 7-15 kNm and 5-8MT." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3097m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and cleaned out rat hole from 3090m MD to 3097m MD in 1m increments." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 3 meter of new formation from 3097m MD to 3100m MD with 2300 lpm, 189 bar, 80 rpm, 12-18 kNm, 3-6 MT and 1.49 sg ECD." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated and conditioned mud prior to perform FIT." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flushed lines and performed line test to 200 bar for 10 minutes." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Performed FIT to 1.60 sg by applying 80 bar down drill string and annulus with 1.32 sg mud for 10 minutes. Pumped 650 liters, bled 600 liters back." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed slow circulation rates." "On 2013-09-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3306m. The activity was categorized as 'drilling -- drill' and lasted for 12.2 hours. Operational details: Drilled and oriented 8 1/2' hole from 3100m MD to 3306m MD with 2200 lpm, 201-210 bar, 110-140 rpm, 10-20 kNm, 1.52-1.55 sg ECD, 6-10 MT. Drilling ROP: 30 m/hr. Average ROP (including connections): 17 m/hr." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3343m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled and oriented 8 1/2' hole from 3306m MD to 3343m MD with 2250 lpm, 201-204 bar, 140 rpm, 16-24 kNm, 1.52-1.53 sg ECD, 7-8 MT. Drilling ROP: 30 m/hr. Average ROP (including connections): 21.1 m/hr" "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3343m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Recycled pumps due to bad survey." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled and oriented 8 1/2' hole from 3343m MD to 3465m MD with 2250 lpm, 203-206 bar, 140 rpm, 13-22 kNm, 1.53-1.55 sg ECD, 7-8 MT. Drilling ROP: 30 m/hr. Average ROP (including connections): 23.2 m/hr." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Performed TD survey." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated hole clean with 2400 lpm, 238-240 bar and 140 rpm." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Performed flowcheck prior to start perform pressure surveys for 15 minutes - well static. Meanwhile: Performed prejob meeting prior to start performing pressure surveys." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Downlinked MWD tools." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3452m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Relogged interval from 3462m MD to 3452m MD with 2100 lpm, 190 bar." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3365m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled wet out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 3452m MD to 3365m MD." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3365m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed sticky test prior to start pressure surveys." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3279m. The activity was categorized as 'drilling -- other' and lasted for 4.2 hours. Operational details: Performed pressure surveys with TesTrak at: - 3362.4 m MD - 3333.9 m MD - 3328.4 m MD - 3323.4 m MD - 3312.9 m MD - 3305.9 m MD - 3298.9 m MD - 3293.4 m MD - 3287.4 m MD - 3279.4 m MD" "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3237m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: Relogged interval from 3253 - 3214m MD with 2200 lpm, 187 bar and 60 rpm." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3237m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flowcheck prior to start pulling out of hole with 8 1/2' bottom hole assembly in open hole for 15 minutes - well static." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3237m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Pumped slug and dropped 3' drift.." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 3237m MD to 3090m MD at 240 sec/stand." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2985m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 3090m MD to 2985m MD at 210 sec/stand." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2985m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed free torque readings for liner hanger reference." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2985m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flow check prior to pull out of hole with 8 1/2' bottom hole assembly in cased hole for 15 minutes - well static." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2750m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 2985m MD to 2750m MD at 210 sec/stand." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 2750m MD to 2400m MD at 180 sec/stand." "On 2013-09-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1926m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 2400m MD to 1926m MD at 120 sec/stand." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1600m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 1926m MD to 1600m MD at 1.5 min/stand. Average pulling speed: 600 m/hr" "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 386m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 1600m MD to 386m MD at 1 min/stand. Average pulling speed: 620 m/hr" "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 386m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flowcheck prior to pull bottom hole assembly through BOP for 15 minutes - well static. Meanwhlie: Performed prejob meeting prior to brake out and lay down 8 1/2' bottom hole assembly." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: Pulled out and laid down 8 1/2' bottom hole assembly to 47m MD. Removed radioactive sources." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Downloaded MWD tools." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled out and laid down 8 1/2' bottom hole assembly from 47m MD to deck." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Removed excess equipment from drill floor. Cleaned and cleared rig floor." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to rig up to run 7' liner." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Rigged up to run 7' liner." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Moved rollers and connected hydraulic power. Meanwhile: Serviced travelling block and dolly." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to run 7' liner." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 60m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Picked up and made up FMS. Picked up shoe to rotary. Verified floats by hosing water through it. Picked up and made up 3 x intermediate joints and landing collar pup to 60m MD. Crane used for picking up shoe track joints due to hydraulic leak on catwalk." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 334m. The activity was categorized as 'completion -- other' and lasted for 3.5 hours. Operational details: Ran 7' liner from 60m MD to 334m MD. Filled liner every 5th joint." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 334m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Experienced problems with casing tong guide arm. Not possible to retract due to faulty shuttle valve. Attempted to repair shuttle valve - no go. Continued in manual mode." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 474m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Ran 7' liner from 334m MD to 474m MD. Filled liner every 5th joint." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 474m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Changed handling equipment and removed power rollers. Meanwhile: Performed prejob meeting prior to pick up and make up 7' liner hanger assembly." "On 2013-09-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 474m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Broke out and laid down fill up crossover. Picked up 7' liner hanger assembly. Made up and installed ball seat and wiper plugs." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 474m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Continued making up 7' liner hanger assembly." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 688m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran in hole with 7' liner on 5 1/2' heavy weight drill pipe from 474m MD to 688m MD. Average trip speed: 285 m/hr." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 688m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Filled pipe." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 6.8 hours. Operational details: Ran in hole with 7' liner on 5 1/2' drill pipe from 688m MD to 3090m MD. Average trip speed: 356 m/hr. Filled running string every 5th stand." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up top drive and circulated one liner volume with 800 lpm and 42 bar. Performed up/down weight measurements." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3435m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Ran in hole with 7' liner on 5 1/2' bottom hole assembly from 3090m MD to 3435m MD. Average trip speed: 230 m/hr. Filled running string every 5th stand." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Established circulation with 400 lpm and 32 bar. Washed down last stand from 3435m MD to 3465m MD. Tagged bottom at 3465 with 5MT. Laid out one single 5 1/2' drill pipe." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up and make up cement head." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Picked up and made up one 3m pup and cement head." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Established circulation with 1200 lpm and 86 bar. Washed in hole with 7' liner on 5 1/2' drill pipe and cement stand and tagged TD at 3465m MD. Pulled up 1.5m to setting depth. Circulated 2 x open hole volume." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Established rotation with 20 rpm and circulated bottoms up with 1200 lpm and 87 bar. Meanwhile: Performed prejob meeting prior to set liner hanger and cement job." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Stopped rotation and flow. Dropped ball and chased same with 500 lpm and 34 bar. Observed landing by pressure increase. Pressured up to 170 bar to set liner hanger. Confirmed liner set by slacking off 30MT." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Applied 10MT weight on liner hanger. Released liner hanger running tool by rotating clockwise. Confirmed liner hanger running tool released by torque indications." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Pumped 10m3 1.32 sg oil based mud at 1500 lpm and 115 bar. Lined up and pumped 15m3 1.38 sg spacer with rig pumps. Closed IBOP and applied 30 bar pressure." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Mixed and pumped 11.2m3 1.90 sg cement slurry. Displaced cement line to drill floor with drill water." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Lined up to mud pumps down string. Displaced cement with 41m3 1.32 sg oil based mud. Bumped the plug with 95.3% effeciency at 100 bar final circulating pressure. Pressured up to 170 bar." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to pump down string with cement unit and closed IBOP. Pressured up to 170 bar to equalize lo-torque. Pressure tested liner to 340 bar for 10 minutes. Observed pressure increase from 340 bar to 345 bar in 10 minutes. Bled off pressure to 5 bar and observed for pressure build up. Pumped a total of 290 liters, bled 300 liters back. Observed pressure build up from 5 bar to 10 bar in 10 minutes - ok. Disconnected lo-torque valve and observed for back flow - no back flow." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pulled up 4.5m to activate packer actorators. Ran in hole to apply weight to set packer. Attempted to apply 40MT weight to set packer. Observed shear at 14MT and 24MT weight. No additional weight increase was oberved. Pulled back to re-activate actorators. Attempted to apply 40MT weight to packer - no go. Pulled back and rotated string at 20 rpm. Ran in hole to set packer with 40MT - ok. Held 40MT on packer in 5 minutes. Slacked off weight." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Closed upper pipe ram and lined up to pump with cement unit down annulus. Pressure tested packer to 340 for 10 minutes - ok. Pumped a total of 1780 liters, bled back same." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Opened upper pipe ram. Applied 30 bar on string and pulled out of hole 5m to release hanger - no pressure release observed. Pulled additional 2 meters - no pressure release observed. Bled off pressure and functioned IBOP close and open and applied 30 bar to string - observed running tool free from PBR." "On 2013-09-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3465m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Increased flow to 2000 lpm and 128 bar. Ran in hole 2 meters to top of PBR. Circulated out excess cement at 2000 lpm and 128 bar." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued circulating out spacer and excess cement at 2000 lpm and 183 bar. Diverted 20m3 spacer and excess cement to slop." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2970m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Broke out cement head, 3 meter pup and 2 drill pipe singles. Laid down same to deck. Inserted 2 x wiper balls and circulated same through string." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Pumped slug. Pulled out of hole with liner hanger running tool on 5 1/2' drill pipe from 2970m MD to 230m MD." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pull out of hole with liner hanger running tool." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed master bushings." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pulled out of hole with liner hanger running tool on 5 1/2' drill pipe and 5 1/2' heavt weight drill pipe from 230m MD to 24m MD." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pulled out of hole and laid down liner hanger running tool to deck." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Cleaned and tidied rig floor." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Performed BOP function test." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked up and made up jetting sub and ran in hole to 15m MD. Jetted BOP with 3000 lpm." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed handling equipment." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up and made up cleanout assembly." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Moved power rollers. Installed 3 1/2' auto slips and dog collar." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up and make up 3 1/2' drill pipe from deck." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 404m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.0 hours. Operational details: Ran in hole with cleanout assembly on 3 1/2' drill pipe to 404m MD. Average trip speed: 101 m/hr." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 404m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 404m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Picked up and made up Well commisioner assembly, circulating sub and well patroler assembly." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 404m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Installed PS 21 slips." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 404m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to run in hole with cleanout assembly." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1040m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Ran in hole with cleanout assembly from 404m MD to 1040m MD (9 5/8' scraper at 600m MD)." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1040m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Established circulation with 1500 lpm, 58 bar and 40 rpm and scraped and cleaned area from 592m MD to 623m MD." "On 2013-09-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2163m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Ran in hole with cleanout assembly from 1040m MD to 2163m MD." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2822m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Ran in hole with cleanout assembly from 2163m MD to 2822m MD." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2822m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up and made up 10 3/4' scraper and drift assembly." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2961m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Ran in hole with cleanout assembly from 2779m MD to 2961m MD (drift at 139m MD), Established circulation with 1200 lpm, 25 bar and 20 rpm. Attempted to drift casing - no go. Observed weight dropped 80MT." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Stopped rotation. Attempted to pass restriction with up to 50MT several times - no go." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2822m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Pulled out of hole with cleanout assembly on 5 1/2' drill pipe from 2961m MD to 2822m MD." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2822m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Prepared to break out and lay down 9.5' drift from cleanout assembly. Broke out 9.5' drift and laid out same." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2978m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Ran in hole with cleanout assemblyfrom 2822m MD to 2978m MD - ok." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3017m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Ran in hole with cleanout assembly from 2978m MD to 3017m MD." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3017m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed master bushings and installed PS21 slips." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3354m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Ran in hole with cleanout assembly from 3017m MD to 3354m MD." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3400m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Made up top drive and filled pipe. Established circulation with 1000 lpm, 81 bar and 40 rpm. Scraped and cleaned production packer setting depth from 2934m MD to 2964m MD." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Continued washing down with cleanout assembly from 3400m MD to 3410m MD and landed polish mill in PBR at 2978m MD. Cleaned and polished PBR with 2000 lpm, 95 bar and 40 rpm." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated and conditioned liner volume with 1.32 sg oil based mud with 2000 lpm and 250 bar." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Sheared out pins in circulation sub with 15MT. Verified ports open. Circulated and conditioned casing and riser volume with 3500 lpm, 250 bar and 90 rpm." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Cycled circulating tool to closed position. Ran in hole and landed on top of PBR. Cycled circulation tool to locked closed position. Pressure tested well commissioner element to 70 bar for 10 minutes - ok. Cycled well commissioner to open position." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Displaced drill string with 22.5m3 base oil. Observed back pressure of 93 bar. Activated well commissioner packer." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Took thermal expansion reference trend by observing pressure for 30 minutes - Pressure increased from 93 bar to 110 bar in 30 minutes." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to perform inflow test." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Lined up to cement unit and pressured up lined to equalize backpressure in standpipe to 110 bar. Opened lo-torque valve to cement unit." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Performed inflow test in steps of 30 bar from 93 bar to 5 bar. Observed pressure for 30 minutes. Pressure increased 2 bar in 30 minutes. Meanwhile: Performed prejob meeting prior to displace well to 1.03 sg brine." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3410m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pressured up string to 100 bar to equalize pressure differential on well commissioner packer. Deactivated well commissioner packer and pulled polish mill 8 m, out of PBR while rotating with 10 rpm." "On 2013-09-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3402m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Pumped wash-train - 15 m3 push pill, 39 m3 cleaning pill, 1 x hole volume packer fluid. Displaced well to 1.03 sg brine with 1700 lpm and 160 bar." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3402m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Continued displacing well to 1.03 sg brine. Observed large amounts of foam in flowline." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3402m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Prepared to perform pressure test. Lined up to cement unit and pressured up same to 20 bar. Opened lo-torque and verified pressure drop." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3402m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pressure tested well to 345 bar for 10 minutes - ok. Pumped a total of 1700 liters, bled 1700 liters back." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3402m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Performed flowcheck for 30 minutes with 1.03 sg brine - well static." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1042m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 5.5 hours. Operational details: Pulled out of hole with cleanout assembly on 5 1/2' drill pipe from 3402m MD to 1042m MD." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1042m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Observed hole not taking correct volume of mud while tripping out - performed flowcheck for 15 minutes with 1.03 sg brine - well static." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1042m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pumped 10m3 1.03 sg brine at 1800 lpm, 64 bar and 90 rpm." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1042m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Performed flowcheck for 30 minutes with 1.03 sg brine - well static." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 464m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Pulled out of hole with cleanout assembly on 5 1/2' drill pipe from 1042m MD to 464m MD." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 464m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed flowcheck for 15 minutes with 1.03 sg prior to pull cleanout assembly through BOP - well static." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Laid down cleanout assembly, magnet, circulation sub and well commissioner." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 420m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed to 3 1/2' handling equipment." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 220m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled out of hole with cleanout assembly on 3 1/2' drill pipe from 420m MD to 220m MD. Laid 3 1/2' drill pipe singles out to cantilever." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 220m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Calibrated HTS arm." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: Pulled out of hole with cleanout assembly on 3 1/2' drill pipe from 420m MD to 10m. Laid 3 1/2' drill pipe singles out to cantilever." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Laid down cleanout assembly to deck." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Picked up and made up 9.5' drift and crossover. Installed PS21 slips." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Ran in hole with 9.5' drift to 139m MD. Attempted to enter 10 3/4' casing with 9.5' drift - no go. Observed 4MT weight. Rotated pipe 1/2 turn and attempted to enter 10 3/4' casing - no go." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pulled out of hole with 9.5' drift on 5 1/2' drill pipe from 139m MD." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Broke out drift assembly and crossover. Laid out same to cantilever." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 312m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Picked up and made up well protector assembly and crossover. Made up 4 stands 5 1/2' drill pipe and magnetosweep, jetting sub and crossover. Ran in hole with cleanout assembly on 5 1/2' drill pipe to 312m MD (with jet at 139m MD)." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 312m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Spaced out and shut well in on middle pipe ram. Displaced choke manifold and poorboy to seawater." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 312m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Displaced riser to seawater at 1500 lpm." "On 2013-09-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 312m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Jetted riser with seawater from 139m MD to 85m MD." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 173m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Jetted BOP and riser from 139m MD to 15m MD." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 173m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Broke out and laid down magnetosweep, jetting sub and crossover to cantilever." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled out of hole with well protector and crossover on 5 1/2' drill pipe from 173m MD. Broke out well protector and crossover and laid down same to cantilever." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Picked up and made up Safelock plug." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 120m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Ran in hole with Safelock plug on 5 1/2' heavy weight drill pipe to 120m MD." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: Ran in hole with Safelock plug on 5 1/2' drill pipe from 120m MD to 607m MD." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to set Safelock plug." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Established circulation with 1100 lpm and washed setting area from 605m MD to 609m MD." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Set Safelock plug by rotating 20 turns clockwise and applying 20MTweight for 5 minutes. Verified plug set by pulling 10MT overpull." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Lined up to cement unit. Pressured up to 30 bar with cement unit by pumping 100 liters of seawater. Volume used indicated open ball valve. Bled down pressure." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Set down 2MT weight on Safelock plug and applied 6kNm torque to shear and close ball valve. Pressured up string to 30 bar using rig pumps. Rotated 1/2 turn clockwise and observed pressure drop." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Pressure tested Safelock plug from below to 345 bar for 10 minutes - ok. Pumped 1471 liters, bled 1463 liters back." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Closed ball valve by rotating 1/2 turn anti-clockwise. Verified ball valve closed by pressuring string up to 345 bar and comparing volumes - ok. Released Safelock running tool." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 607m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Spotted 5m3 high visc pill on top of Safelock plug and displaced same with 2000 lpm, 12 bar and 40rpm." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Pulled out of hole with Safelock running tool on 5 1/2' drill pipe from 607m MD to 140m MD." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Displaced riser and BOP to seawater with 2200 lpm and 10 bar." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Pulled out of hole with Safelock running tool on 5 1/2' drill pipe from 140m MD. Laid out Safelock running tool to cantilever." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Closed shear ram. Pressure tested Safelock plug from above to 345 bar for 10 minutes. Pumped 723 liter, bled 723 liters back." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Cleaned and tidied rig floor." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up and made up wearbushing retrieval tool and jet sub to 5 1/2' heavy weight drill pipe." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Ran in hole with wearbushing retrieval tool and jet sub to 139m MD. Jetted wellhead area with 1400 lpm and 8 bar." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Landed off with wearbushing retrieval tool with 5MT weight. Picked wearbushing free with 39MT overpull." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled out of hole with wearbushing from 139m MD. Laid out wearbushing to cantilever. Broke out and laid down wearbushing running tool to cantilever. Inspected wearbushing and found ID to 9.5'." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Picked up and made up 9.5' drift and crossover to 5 1/2' drill pipe." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 575m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Ran in hole with 9.5' drift on 5 1/2' drill pipe to 575m MD - ok." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Pulled out of hole with 9.5' drift on 5 1/2' drill pipe from 575m MD. Laid out same to cantilever." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up and made up lockdown sub." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ran in hole with lockdown sub on heavy weight drill pipe to 139m MD. Installed lockdown sub by landing off with 7MT and rotating 4 1/2 turns clockwise. Observed drop to verify installed lock down assembly." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested lockdown sub to 207 bar for 10 minutes - ok. Pumped 262 liters, bled 260 liters back." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Applied 30MT overpull - ok. Rotated 5 turns clockwise to release running tool." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled out of hole with lockdown assembly running tool from 139m MD, and laid down same to cantilever." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Bled down koomey-unit and prepared to pull diverter. Meanwhile: Performed general maintanence." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pull diverter element and slick joint." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: Pulled master bushings and outer ring and installed lift eyes to diverter. Pulled diverter and landed on set back." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: Pulled slick joint and landed in set back. Installed master bushings and ring." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to nipple down BOP." "On 2013-09-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Nippled down BOP." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Continued nippling down BOP and placed back on carrier." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to rigging up to pull high pressure drilling riser." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Rigged up to pull high pressure drilling riser. Picked up and made up claxton tool to 5 1/2' drill pipe. Landed off claxton tool to NT-2 connector. Verified make up by applying 5MT overpull." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to rig down tensioning system." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Rigged down tension cylinders and tension ring. Rigged up sheaves for running guide wires. Meanwhile: Prepared 24' elevator, C-plate and bails on rig floor." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Ran guide wire on tugger to seabed. ROV attached same." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran hot stab to seabed and installed same in tieback connector with ROV." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pressured up hot stab connection to 3000 psi. Unlatched tieback connector and picked riser off wellhead." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Retrieved hotstab and reinstalled dummy stab." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up clear of wellhead and retrieved VX gasket with ROV. Installed debris cap on wellhead." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pull out of hole with riser." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled up with tieback connector and high pressure drilling riser. Racked back 5 1/2' drill pipe stand. Removed crossover." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed master bushings and outer ring. Prepared to install riser spider and hydraulic hoses." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to install riser spider." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed riser spider and function tested same." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pull high pressure drilling riser out of hole and lay out same to cantilever." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up BOP joint and closed spider dogs. Installed C-plate and side door elevator onto spider. Landed off BOP joint in side door elevator on top of spider." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Disconnected BOP joint. Laid out BOP joint and claxton tool to cantilever." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed BX-elevator and attached bails to side door elevator. Picked up tension joint and set in spider." "On 2013-09-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Disconnected tension joint and laid out same to cantilever." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Pulled double riser joint (upper pup and splash zone joint). Disconnected same and laid out to cantilever." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pulled double riser joint (standard joint #4 and #7). Disconnected same and laid out to cantilever." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Pulled single joint #6. Disconnected same and laid out to cantilever." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Retrieved guidelines from seabed." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pulled single joint #3. Disconnected same and laid out to cantilever." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pulled lower riser pup joint. Disconnected same and laid out to cantilever." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Laid out stress joint and tieback connector to cantilever." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Transferred tension rings and wellhead equipment to rig floor." "On 2013-09-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 10.5 hours. Operational details: Waited on weather. Meanwhile: Performed general maintenance. Serviced forward and aft pipe racking systems." "On 2013-09-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 24.0 hours. Operational details: Waited for weather. Time: Significant waveheight: Wind speed: 00:00 1.7 m 8.0 kt 06:00 1.4 m 23.0 kt 12:00 4.2 m 34.0 kt 18:00 5.0 m 21.0 kt 24:00 3.2 m 17.0 kt Meanwhile: Performed general maintenance. Split tension ring. Moved tension ring to moon pool. Installed tension ring. Performed 5 year choke manifold service. Installed top cover onto F-1 split hatch. Greased and inspected top drive and travelling block. Housekeeping." "On 2013-09-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 24.0 hours. Operational details: Waited for weather for running production riser. Time: Significant waveheight: Wind speed: 00:00 3.2 m 17.0 kt 06:00 2.9 m 8.0 kt 12:00 2.3 m 15.0 kt 18:00 1.9 m 16.0 kt 24:00 3.6 m 22.0 kt Meanwhile: Performed general maintenance. Continued performing 5 year choke manifold service. Cleaned pits. Lifted wing valves for multibowl to rig floor. Lowered same through rotary. Changed bladders on Koomey bottles. Pressure tested BOP on stump to 345 bar. Housekeeping." "On 2013-09-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 24.0 hours. Operational details: Waiting on weather for running production riser. Time: Significant waveheight: Wind speed: 00:00 3.6 m 22.0 kt 06:00 3.6 m 24.0 kt 12:00 3.5 m 22.0 kt 18:00 2.8 m 18.0 kt 24:00 2.6 m 13.0 kt Meanwhile: Changed out wires on moonpool tuggers. Changed oil cooler on top drive. Greased manifolds. Performed drive chain check on mud pump #1. Performed general mainenance." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 11.0 hours. Operational details: Waiting on weather. Time: Significant waveheight: Wind speed: 00:00 2,5 m 14.0 kt 06:00 2,2 m 9.0 kt At 09:40 hrs commenced shut down of production. At 11:00 hrs production shut down completed. Meanwhile: Pressure tested kill and choke manifold, standpipe manifold, upper and lower IBOPs. Performed general maintenance and housekeeping. Troubleshot leak on TDS oil cooler, repaired same. Prepared riser guide funnel on deck." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to run riser guide funnel." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Installed riser guide funnel on wellhead." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Waited on the crane handling supply vessel. Meanwhile performed general maintenance and housekeeping." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to removal of split hatch." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed split hatch. Meanwhile: ROV installed VX ring. Performed pre-job meeting prior to make up landing string" "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed lifting nubbing onto riser tension joint on deck." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to run riser." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up tieback connector and stress joint and landed same in rotary. Picked up and made up riser pup joint to stress joint. Installed fairings. Lowered production riser through rotary to test connector." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Function tested tieback connector." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Picked up standard riser joint #1 made up to riser pup joint. Pressure tested flange connection." "On 2013-09-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed flange protection fairings." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed guide wires and ROV hooks." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up standard riser joint #2 and made up to riser joint #1. Inspected seal faces and installed IX-14 ring gasket. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port, ok. Installed fairings." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran guideline wires to seabed and attached same to template." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.8 hours. Operational details: Waiting on weather. Time: Significant waveheight: Wind speed: 03:00 2,5 m 22,0 kt 06:00 2,2 m 16,0 kt 09:00 2,1 m 10,0 kt Meanwhile performing planned maintenance and housekeeping. Replaced faulty fingers in DP fingerboard. Performed pre-job meeting prior to run production riser." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 67m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Picked up standard riser joint #3 and made up to riser joint #2. Inspected seal faces and installed IX-14 ring gasket. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port, ok. Held pre-job meeting prior to run through splash zone. Lowered riser through splash zone and sat in riser spider. Installed fairings." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 81m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up standard riser joint #4 and made up to riser joint #3. Inspected seal faces and installed IX-14 ring gasket. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port, ok. Lowered riser and sat in riser spider. Installed fairings." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 96m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up riser splash zone joint and made up to riser joint #4. Inspected seal faces and installed IX-14 ring gasket. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port, ok. Lowered riser and sat in riser spider. Installed fairings." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 102m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up upper riser pup joint and made up to riser splash zone joint. Inspected seal faces and installed IX-14 ring gasket. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port, ok. Lowered riser and sat in riser spider. Installed fairings." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Picked up riser tension joint and made up to splash zone joint. Inspected seal faces and installed IX-14 ring gasket. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port, ok. Lowered riser and sat in riser spider. Installed fairings." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Disconnected riser running tool from riser tension joint and cleaned seal face." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up pre-made landing string." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with oncoming crews." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up pre-made riser running tool to tension joint." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to landing production riser." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up TDS to riser running tool and removed hang off plates." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Lowered riser to safe distance above riser landing guide funnel. Verified VGX ring installed with ROV. Stabbed riser into vertical guide and onto WH." "On 2013-09-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed riser guide funnel." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Continued to remove riser guide funnel." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered hot stab and connected same to tieback connector using ROV." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Landed off tieback connector on wellhead with 15 Ton. Locked connector by applying 3000 psi until stroke indicator indicated fully set." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed 10 Ton overpull test to verify connector fully latched." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Recovered riser guide funnel to deck. Att: 04:15 hrs started production as per SIMOPS procedure. Meanwhile: Removed riser spider from rotary. Filled riser. Confirmed line up from cement unit and tested lines to 20 / 200 bar - 5 / 10 min." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pressure tested production riser to 20 / 200 bar - 5 / 10 min. Pumped 670 liter. Took 650 liter return." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Flushed tieback connector control lines. Sat all valves to parking position. Recovered hot stab." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Retrived guide line wires to surface." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: Installed riser centralizers, tension ring and tension cylinders." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Performed pre-job meeting. Performed 3D survey to verify correct cutting height of production riser." "On 2013-09-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 7.2 hours. Operational details: Waited on parts for cutting tool. Meanwhile performed planned maintenance and housekeeping. Moved multi bowl to drill floor. Transferred X-mass tree from deck to moonpool." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.8 hours. Operational details: Waited on parts for cutting tool. Meanwhile performed planned maintenance and housekeeping." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Cut production riser." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled cut off piece to drill floor and laid out same." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Bewelled production riser edge. Meanwhile: Picked up BOP riser joint and Claxton tool." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up multibowl and landed at well center and made up same to BOP joint. Performed pickup test to 15 cm above deck,ok." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed pre-job meeting. Informed production to shut down well F11 & F12." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared to remove master bushings and cover from split hatch while production shuts down." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Removed master bushings and cover from split hatch. Ran multi bowl and BOP joint assembly through rotary. Installed master bushings. Picked up single and ran in with multibowl assembly. Removed master bushings. Retrached TDS to align multibowl. Landed out multibowl." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Tested multibowl BT and FS seals. Energized plastic in upper and lower BT seals and tested same." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Energized multibowl slips. Performed 5 Ton overpull test, ok." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed hatches around production riser." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Erected scaffolding around Claxton tool in moonpool. Meanwhile made up annulus valves on multibowl. Tested annulus valves to 30 / 345 bar - 5 / 10 minutes. Replaced damaged fitting on Claxton tool." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Released Claxton tool. Pulled out with Claxton tool and laid down same to cantilever. At 19:00 informed production to shut down well F14." "On 2013-09-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Performed pre-job meeting. Moved BOP to well center and landed same onto riser. Made up NT2 connector. Ran slick joint and made up same. Installed diverter. Connected tension system. At 21:15 informed production to start." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Connected tension system. Meanwhile rigged down diverter handling equipment." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Filled riser with seawater." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up bowl protector RT and made up to 5 1/2' DP. RIH and installed bowl protector at 20,53 meter. POOH with RT." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Picked up jetting sub and RIH on 5 1/2' DP to 150 meter. Closed upper pipe ram. Pumped seawater at 550 liter/min through choke and kill lines until clean returns observed. Opened upper pipe ram. Pumped 14 m3 Hi-vis pill at 2000 liter/min, 5 bar and chased same with 3,5 m3 seawater. RIH to 162 meter and circulated with seawater at 3000 liter/min, 25 bar, 5 rpm. POOH with jetting sub." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Picked up and RIH with annulus insert retrieval tool. Engaged annulus insert at 139,95 meter. Released annulus insert with 6000 Nm. Displaced riser to brine. POOH with annulus insert retrieval tool and insert, laid down same." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH with bowl protector retrieval tool and retrieved bowl protector. POOH with bowl protector and RT." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rig up handlling equipment." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Rigged up 10 3/4' handling equipment for tie-back casing." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to run tie-back connector." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Picked up 10 3/4' tie-back connector, inspected same, ok. Picked up and RIH with 10 3/4' tie-back string as per running tally from surface to 119,34 meter." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 10 3/4' surface casing hanger assembly with adjustment sub and continued to RIH." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Tagged land off point with 3 Ton. Landed off tie-back string at 139,88 meters." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rotated string to engage threads in tie-back adapter." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released riser RT and POOH with same. Meanwhile drained riser." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Performed pre-job meeting prior to rig down handling equipment. Rigged down handling equipment for 10 3/4' tie-back casing and cleared drill floor. Rigged up 5 1/2' handling equipment." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up and made up tie-back torque tool. RIH with tie-back connector torque tool on 5 1/2' DP. Landed and engaged torque tool in tie-back adapter at 139,55 meter and sat down 3 Ton. Made up Tie-back connector to 9500 Nm. POOH with tie-back connector torque tool on 5 1/2' DP." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged 10 3/4' handling equipment for tie-back casing. Performed pre-job meeting." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up casing hanger landing string and RIH to top of casing hanger at 20,5 meter. Engaged same." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged up swedge and hose for tie-back adapter test. Flushed lines and tested lines to 345 bar - 5 minutes. Pressure tested tie-back adapter to 20 / 345 bar - 5 / 10 minutes. Observed B annulus at multibowl. Pumped 486 liter, bled back 486 liter. Rigged down swedge and hose." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed to 5 1/2' DP handling equipment." "On 2013-09-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up adjustable sub setting tool and RIH to 28,3 meter." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Applied 140 bar to adjustable sub setting tool, picked up to 1 Ton overpull and bleed off pressure. Turned string 14 turns with 5 rpm, 200-1500 Nm. No drop observed on casing." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Repositioned string at 28,3 meter. Applied 150 bar, picked up to 1 Ton and bled off pressure. Turned string 14 turns with 5 rpm, 200-1500 Nm. No drop observed on casing." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with adjustable sub setting tool and inspected same, ok." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with adjustable sub setting tool and RIH to 28,3 meter." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Applied 140 bar, picked up to 7 Ton and bleed off pressure. Turned string 14 turns and picked up to 35 ton overpull. Continued to turn untill 9000 Nm torque achieved. Observed correct movement on casing stickup and on annulus port on multibowl." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH with adjustable sub setting tool. Changed to 10 3/4' handling equipment." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Made up swedge and hose, tested same. Pressure tested adjustable sub internal seal to 20 / 345 bar - 5 / 10 minutes. Pumped 486 liter, bled back 486 liter." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Disengaged casing hanger running tool. POOH and laid down casing hanger landing string. Rigged down 10 3/4' handling equipment." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Picked up 10 3/4 MS-T seal assembly RT and made up same to 5 1/2' DP. Connected hydraulic lines to RT and flushed through same. Function tested 10 3/4' MS-T seal assembly. Installed MS-T seal on RT. RIH with seal assembly on 5 1/2' DP, landed off at 20,75 meter. Locked seal assembly into riser, confirmed lock with 10 Ton overpull. Set MS-T seal assembly." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Tested MS-T seal assembly to 345 bar - 10 minutes through multi bowl port. POOH with 10 3/4' MS-T seal assembly RT and laid down same." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up bowl protector RT and made up to 5 1/2' DP. RIH and installed bowl protector at 20,53 meter. POOH and laid down bowl protector RT." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to line up and pressure test." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed shear rams and lined up to test. Pressure tested BOP connection against safe lock plug to 20 / 345 bar - 5 /10 minutes. Pumped 478 liter, bled back 448 liter. Opened shear rams." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to retrieval of Safe lock plug." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 3.0 hours. Operational details: Picked up Safe Lock plug RT and made up to 5 1/2' DP. RIH with Safe Lock plug RT on 5 1/2' DP from surface to 601 m with restricted speed. Stopped operation due to contamination of active pit." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Cleaned contaminated pit. Prepared new brine." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: At 601 meter made up TDS and commenced circulation with 200 liter/min, 2,8 bar. Pulled back to 591 meter." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Increased flow rate to 2000 liter/min, 7-8 bar and displaced hi-visc pill out of well Decreased rate to 300 liter/min, 2-3 bar and washed back down to 601,6 meter. Continued to wash down with 150 liter/min to top of plug at 607,7 m." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: Latched onto plug. Set down 20 Ton on plug, rotated string 1/2 RH turn, took 15 Ton overpull. Slacked off 2 Ton weight and applied 35 bar, observed pressure drop to 15 bar, bleed off pressure to 0 bar. Took 2 ton overpull and rotated 24 right hand turns to release plug. Performed flow check for 10 minutes, ok. RIH to below plug setting point to ensure plug was retrieved and free, ok. POOH with Safe Lock plug on 5 1/2' DP from 611 m to surface with restricted speed. Inspected Safe Lock plug and RT, laid down same to cantilever." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up bowl protector RT and made up same to 5 1/2' DP. RIH to 21,1 meter and retrieved bowl protector. POOH with bowl protector." "On 2013-09-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Cleaned and cleared rigfloor. Performed pre-job meeting prior to rig up tubing equipment." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Changed to 7' handling gear, BX elevators, installed rotator. Installed 7' casing tong and tested same. Rigged up cable drums on rigfloor and installed sheave for DHPG. Prepared completion assembly #1 and #2 on deck. Installed Vario spider slips and tested same." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with all involved personnel prior to run completion string." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 59m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Picked up and RIH 7' completion from surface to 59 meter. Assembly #1 with 7' perforated stem and mule shoe. Assembly #2 with pre installed EVO plug and auto fill valve. Assembly #3 with BOT Granite packer. 2 ea. plain 7' tubing joints. Assembly #4 with DHPG. Observed 1 rejected joint." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 78m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Picked up and RIH assembly #4 with DHPG. Installed 1 ea. plain 7' tubing joint and RIH to 78 meter. Terminated cable to Down Hole Pressure Gauge. Function tested DHPG." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 78m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to RIH with completion string." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 78m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Rigged down DHPG test equipment." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 203m. The activity was categorized as 'completion -- completion string' and lasted for 3.2 hours. Operational details: RIH with 7' tubing from 78 m to 203 m. Average running speed 3,2 joints/hr." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 203m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Replaced tong die mesh due to poor grip. Broke out and checked connection, made up same." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 510m. The activity was categorized as 'completion -- completion string' and lasted for 4.2 hours. Operational details: RIH with 7' tubing from 203 m to 510 m. Average running speed 6,0 joints/hr." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 510m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Replaced tong die mesh due to poor grip. Broke out and checked connection, made up same." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 650m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: RIH with 7' tubing from 510 m to 650 m. Average running speed 5,2 joints/hr. Observed trouble with HTS." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 650m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Repaired sensor on HTS." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 697m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: RIH with 7' tubing from 650 m to 697 m. Average running speed 4 joints/hr." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 697m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to RIH with completion string." "On 2013-09-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1096m. The activity was categorized as 'completion -- completion string' and lasted for 4.8 hours. Operational details: RIH with 7' tubing from 697 m to 1096 m. Average running speed 7 joints/hr." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1108m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: RIH with 7' tubing from 1096 m to 1108 m. Average running speed 4 joints/hr." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1600m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Replaced make up tong dies." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1662m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: RIH with 7' tubing from 1108 m to 1662 m. Average running speed 7,7 joints/hr." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1662m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to RIH with completion string." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1873m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: RIH with 7' tubing from 1662 m to 1873 m. Average running speed 6,4 joints/hr." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1873m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Emptied trip tank. Greased automatic slips." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2482m. The activity was categorized as 'completion -- completion string' and lasted for 6.8 hours. Operational details: RIH with 7' tubing from 1872 m to 2482 m. Average running speed 7,5 joints/hr." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2482m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Performed pre-job meeting" "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2482m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: Picked up and made up assembly #5 DHSV and made up same to string. RIH with completion string from 2482 m to 2490 m. Installed and terminated DHSV control lines. Tested DHSV control lines to 520 bar. Tested DHSV control lines to 345 bar and maintained DHSV open while RIH from 2490 m to 2502 m." "On 2013-09-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2759m. The activity was categorized as 'completion -- completion string' and lasted for 3.8 hours. Operational details: RIH with 7' tubing from 2502 m to 2759 m. Average running speed 5,7 joints/hr." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2759m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Flow checked well for 10 min, ok." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2958m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: RIH with 7' tubing from 2759 m to 2958 m. Average running speed 7,4 joints/hr." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2958m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Recorded up / down weights, 181 / 145 Ton. Changed to 5 1/2' DP elevators. Picked up landing string and made up to 7' tubing. Removed automatic slips. Installed masterbushings and manual slips." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2983m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Performed pre-job meeting prior to space out run. RIH with 7' tubing from 2958 m to 2980 m At 2980 m commenced washing down with at 200 liter/min, 4,6 bar Stung into PBR at 2981 m, no pressure increase observed, stopped pumps. Continued to RIH and sheared pins with 6,1 Ton down on PBR NO-GO ring. Marked pipe and POOH to up weight + 0,80 meter." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: POOH with 5 1/2' DP landing string. Changed to 7' elevator inserts. Picked up and made up 3,0 meter space out pup." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: Picked up and made up tubing hanger to space out joint. Landed tubing hanger in C-plate. Broke out TH handling tool. Installed tubing hanger running tool and made up landing string. Terminated and tested lines to 520 bar - 10 minutes, ok." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Picked up and made up landing joints to string. RIH with hanger and landed same on 7' landing string. Observed 1,32 meter stick up. Verified correct hanger seal integrity by testing to 70 bar - 5 min through ports on multi-bowl. Engaged tubing hanger lock down ring. Performed pull test to 15 Ton overpull, ok. Meanwhile drained riser." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Pressure tested liner hanger seal to 35 / 345 bar - 5 / 10 min." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Rigged up swedge and cement hose, tested same to 345 bar - 10 min." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Pressure tested control lines to 570 bar - 10 minutes." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Dropped ball for setting packer." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Circulated ball down with 3500 liter/min, 29 bar, pressure increased to 70 bar at landing. Held 70 bar pressure for 5 min to check integrity of completion string." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Increased pressure to 275 bar and held same for 15 minutes to set packer. Meanwhile observed vent line on annulus A. Observed leaking cap on swedge." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Bled off pressure and replaced gasket on leaking cap for swedge." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Pressure tested tubing to 345 bar - 30 minutes. Bled pressure down to 280 bar. Closed DHSV. Bled pressure down to 210 bar and performed low pressure inflow test, 70 bar, 30 min. Bled pressure down to 10 bar and performed high pressure inflow test, 280 bar, 10 min. Bled pressure back to 0 bar and opened DHSV." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Lined up and tested connection from cement unit to A annulus. Performed pressure test of production packer though A annulus to 35 / 345 bar, 5 / 10 min." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rig up and run wilreline." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Rigged up wireline sheaves and equipment. Made up wireline tool string." "On 2013-09-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 3.2 hours. Operational details: RIH with wireline tool string and retrieved EVO plug." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.8 hours. Operational details: While POOH EVO plug stopped inside DHSV, jarred twice and continued to POOH to surface. Laid out EVO plug and wireline tool string. Laid down wireline sheaves and equipment." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Pressure tested line up from cement unit to drill floor to 355 bar. Pressure tested production packer from below to 345 bar- 30 minutes. Pumped 1201 liter, bled back 1201 liter. Closed DHSV. Rigged down test equipment." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held pre-job meeting. Disconnected tubing hanger RT by rotating 9 turns clockwise. POOH with 7' landing string and tubing hanger, laid out same." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Rigging down tubing handling and completion equipment." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Picked up and made up BPV running tool to 5 1/2' DP. RIH from surface to 20,55 meter and installed BPV plug. POOH and laid down RT." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.2 hours. Operational details: Performed pre-job meeting prior to nipple down BOP. At 09:00 production was shut down. Rigged up handling equipment for nipple job on rigfloor. Nippled down diverter, pulled same to rigfloor and secured. Removed riser tension cylinders. Disconnected BOP from HP riser and skidded same to stump. Pulled riser to rigfloor." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Terminated wellhead control lines. Prepared XMT." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Removed masterbushings and hatch in moonpool. Ran down with spacer spool and landed same on multi-bowl. Made up spool piece. Tested connection to 35 / 345 bar 5 / 15 minutes." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed pre-job meeting." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed F-1 hatch covers. Lowered down flow line spool piece to well head deck." "On 2013-09-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Performed housekeeping and maintenance on drill floor. Worked with termination and test of control lines for DHSV and DHPG." "On 2013-09-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Performed housekeeping and maintenance on drill floor. Worked with termination and test of control lines for DHSV and DHPG." "On 2013-09-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held pre-job meeting prior to installation of XMT. Transferred XMT from overhead crane to TDS. Ran down with XMT to 15 cm above land off." "On 2013-09-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: Landed and orientated XMT. Closed hatches above well. Installed clamp on XMT connection. Installed flow line spool to ensure correct line up. At 06:00 hrs informed Production to restart production according to SIMOPS. Meanwhile: Performed housekeeping and maintenance on drill floor. Rigged up hose and valves for pressure testing." "On 2013-09-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up HXT clamp connection and tested same." "On 2013-09-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Prepared for handing over well to Production for commissioning. Well handed over to Maersk Production at 14:00 hrs." "On 2013-09-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 10.0 hours. Operational details: Prepared wire line equipment. Pressure tested TDS." "On 2013-09-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: Prepared wire line equipment. Pressure tested TDS. Performed slip & cut. At 04:45 hrs well was handed over from Maersk Production to Drilling." "On 2013-09-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Erected scaffolding around XMT. Removed XMT cap. Retrived BPV and laid out same." "On 2013-09-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Rigged up wire line equipment, installed X-over on XMT." "On 2013-09-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to rig up." "On 2013-09-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 4.8 hours. Operational details: Rigged up wire line riser and BOP. Erected scaffolding around WL BOP in moonpool. Installed grease head. Hooked up control lines for WL BOP. Filled WL riser with MEG and tested rig up to 30 / 200 bar - 5 /10 minutes." "On 2013-09-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 12.0 hours. Operational details: Rigged up and prepared equipment for perforation. Made up perforation tool string. Meanwhile: Prepared to pressure test BOP on stump. Pressure tested stand pipe manifolds." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 4.5 hours. Operational details: Rigged up and prepared equipment for perforation. Made up perforation tool string. Meanwhile: Performed housekeeping and planned maintenance in all drilling areas. Pressure tested stand pipe manifolds." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.5 hours. Operational details: Rigged up and prepared equipment for perforation. Made up perforation tool string and tested same. Meanwhile: Filled lubricator with MEG. Leak tested WL lubricator and Quick Test Sub rig up to 30 / 200 bar - 5 /10 minutes. Observed WL string stuck." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Observed WL string stuck.Not able to pull through lubricator tubes. Broke QTS sub and released wire and tool. Re-tested WL lubricator and Quick Test Sub rig up to 30 / 200 bar - 5 /10 minutes." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: Broke off lubricator. Performed pre-job safety meeting prior to handling of explosives." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 3.0 hours. Operational details: Picked up and made up perforation gun assembly #1. Made up and leak tested WL lubricator and Quick Test Sub rig up to 30 / 200 bar - 5 /10 minutes." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 5.2 hours. Operational details: RIH with perforation gun assembly #1 from surface to 3360 m. WHP 18 bar." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Correlated across perforation interval. Positioned gun with top shot at 3296 m. WHP 36 bar, bled down to 1,2 bar." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.2 hours. Operational details: Perforated interval between 3296 m to 3304 m. WHP stabilized at 32 bar." "On 2013-09-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: POOH with perforation gun assembly #1 from 3304 m to 1361 m." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: POOH with perforation gun assembly #1 from 1361 m to 250 m." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job safety meeting prior to handling of explosives." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: POOH with perforation gun assembly #1 from 250 m to surface. Closed well, inflow tested and bled down to 0 bar." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Broke lubricator. Laid down perforating BHA on deck." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 4.2 hours. Operational details: Re-build cable head and prepared guns for perforation run #2" "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job safety meeting prior to handling of explosives." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Picked up and made up perforation gun assembly #2. Made up and leak tested WL lubricator and Quick Test Sub rig up to 30 / 200 bar - 5 /10 minutes." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH with perforation gun assembly #2 from surface to 3378 m. WHP 35 bar." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Correlated across perforation interval. Positioned gun with top shot at 3284 m. WHP 32 bar." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.2 hours. Operational details: Perforated interval between 3278 m to 3284 m. WHP stabilized at 32 bar." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Correlated across perforation interval. Positioned gun with top shot at 3245 m. WHP 32 bar." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.2 hours. Operational details: Perforated interval between 3251 m to 3245 m. WHP stabilized at 32 bar." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: POOH with perforation gun assembly #2 from 3284 m to 180 m." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job safety meeting prior to handling of explosives." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: POOH with perforation gun assembly #2 from 180 m to surface. Closed well, inflow tested and bled down to 20 bar. Observed blockage in bleed down line." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Unblocked the bleed down line." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Bled down pressure to 0 bar." "On 2013-10-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Broke lubricator. Laid down perforating BHA on deck. Cut cable and rebuild head." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.5 hours. Operational details: Cut cable and rebuild head. Prepared for perforation run # 3." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Performed pre-job safety meeting prior to handling of explosives." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Picked up and made up perforation gun assembly #3 and stabbed lubricator." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Made up and leak tested WL lubricator and quick test sub to 30/200 bar 5/10 min." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.8 hours. Operational details: Opened well as per procedure. RIH w/ perforation run #3 (interval 3254 - 3262 m) as per program and SLB/Aker procedure." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Correlated across perforation interval. Positioned gun with top shot at 3254 m. WHP 32 bar." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Perforated interval 3254 - 3262 m. No indication of guns firing. Attempted to fire several times, no success." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: POOH from 3262 m to 200 m, established barriers prior to pulling guns to surface." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to handling of unfired guns." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: POOH from 200 m to surface. Closed HMW on XMT, inflow tested same and bleed pressure in WL riser as per procedure." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Broke lubricator and disconnected fire head from gun section." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: L/D gun section on HTS. SLB investigated gun section/fire head." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for making up new perforation toolstring." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Picked up and made up new gun assembly #3 re-run. Stabbed lubricator and M/U same, tested quick test sub to 30/200 bar fo 5/10 min." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Opened well as per procedure. RIH w/ perforation run #3 re-run (interval 3254 - 3262 m) to 3375 m." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Correlated across planned perforation interval. Positioned gun with top shot at 3254 m. Reduced WHP from 102 bar to 35 bar." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval 3254 - 3262 m and observed good indication that guns had been fired. WHP 35 bar." "On 2013-10-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: POOH with perforation assembly from 3262 m to 200 m. WHP 35 bar." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Closed and inflow tested HMV, good test. Drained and flushed riser with nitrogen. Broke lubricator. Disconnected fired gun section from tool string. All shots fired. L/D assemblies on deck." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.0 hours. Operational details: Layed down lubricator section with grease injection head on HTS. Prepared for double lift of wireline riser with elevators and lifting cap. Disconnected riser and suspended same in slips and TDS. Installed tree cap." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 4.0 hours. Operational details: Removed split hatches and installed permanent hatch on F-1 slot. Secured bolts on hatch and removed moonpool access scaffold. Prepared for skidding cantilever package." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Installed and pressure tested hose to KWV, 20/220 bar for 5/10 mins." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting with all involved personel for testing of Xmas tree." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 3.0 hours. Operational details: Prepared and connected hoses and lines for testing of Xmas tree. Meanwhiled continued preparation for skidding of cantilever package." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Pressure tested tree cap to 30/200 bar for 5/10 min. Pressure tested tree SV to 30/200 bar for 5/10 min." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Pumped 1 m3 MEG and displaced with 2 m3 packer fluid, 200lpm / 200 bar." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: TOFS, observed discrepancy in test pressure. Confirmed correct test pressure and prepared permit for tree test to 30/345 bar." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Pressure tested surface line, tree cap and SV to 30/345 bar for 5/10 min." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Pumped remaining 6 m3 packer fluid w/ 200lpm 300 - 330 bar (pumped 8 m3 packer fluid in total). Monitored and bled off WHP f/330 - 90 bar." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Monitored and bled off WHP f/90 - 60 bar while waiting on decision for next operation." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Decision made to perform additional perforation run on F-1 B. Terminated final pressure tests on Xmas tree. Bled down pressure to 35 bar, closed DHSV. Bled pressure above DHSV to 5 bar, closed HMV and SV." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed TBT for handling hatches in moonpool." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Removed permanent hatch from F-1 slot. Installed split hatches." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for installation of wireline riser." "On 2013-10-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.0 hours. Operational details: Removed tree cap. Lowered and landed W/L riser on tree. M/U riser to tree." "On 2013-10-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.0 hours. Operational details: Re-installed 7/16' cable drum on W/L unit. Prepared grease injection head and cable head." "On 2013-10-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 5.0 hours. Operational details: Leak tested W/L riser rig-up to rig floor with 30/200 bar for 5/10 min. M/U GIH to lubricator section. Schlumberger re-build cable head." "On 2013-10-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 3.5 hours. Operational details: Prepared toolstring for run #4. Opened and inspected S6 valve on standpipe manifold, stenciled numbers on manifolds and main deck hatches. Performed general rig maintenance and high wind checks." "On 2013-10-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: P/U lubricator, M/U wireline toolstring and stabbed lubricator on riser section." "On 2013-10-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Pressure tested quick test sub and lubricator section to 30/200 bar for 5/10 min. Bled down pressure, lifted lubricator and set back same." "On 2013-10-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.8 hours. Operational details: Waited on new seal rings for perforation toolstring, ETA Maersk Inspirer 19:00 hrs w/ helicopter. Meanwhile performed general rig maintenance. Opened BOP ram doors. Inspected and measured rams and cavities." "On 2013-10-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.0 hours. Operational details: Waited on new seal rings for perforation toolstring. Helicopter cancelled due to fog. New ETA for seal rings 07:00 hrs w/ supply boat Rem Hrist. Meanwhile performed general rig maintenance. Cleaned and inspected all BOP seals prior to closing ram doors. Closed ram doors and prepared BOP for pressure testing. Installed scaffold under NT-2 connector. Torqued up bolts on standpipe valve #6." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 7.0 hours. Operational details: Waited on new seal rings for perforation toolstring. Meanwhile performed general rig maintenance. Prepared BOP for pressure testing. Performed pressure testing of standpipe manifold and BOP." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: Schlumberger installed seal rings and tested tools on deck." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Placed barriers prior to handling explosives. M/U guns for perforation run#4 to toolstring. Stabbed lubricator." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Leak tested lubricator/QTS to 30/200 bar 5/10 min. Opened well as per procedure. WHP 35 bar." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.8 hours. Operational details: RIH w/ perforation run #4 to 3294 m." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Correlated across interval 3294 - 2979 m. Positioned gun with top shot at 3273 m. Bled WHP from 100 to 35 bar." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.5 hours. Operational details: Fired guns at first interval from 3273 - 3274,5 m. Good indications of guns beeing fired. WHP 37 bar. Positioned guns for second interval from 3288 - 3294 m. Fired guns at second interval, good indication. WHP 37 bar." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: POOH with perforation run #4 from 3288 m to 250 m." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Placed barriers and made PA announcement for handling explosives. POOH from 250 m into tool catcher." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Closed SV, SIWHP 37 bar. Closed HMV. Bled down pressure to 5 bar. Inflow tested HMV for 10 min. Good test." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Bled pressure in Xmas tree, riser and lubricator to zero. Flushed riser and lubricator with nitrogen." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Hold TBT. Bled pressure in lubricator, broke same. Hung off guns on clamp and layed down firing head. Cleaned and layed down guns. All shots fired." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Removed QTS and installed lifting cap on riser. Layed down lubricator and removed grease injection head." "On 2013-10-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 0.8 hours. Operational details: Disconnected wireline riser and suspended same with the TDS. Installed tree cap. Removed split hatches from F-1 slot." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 1.5 hours. Operational details: Installed permanent hatch on F-1 slot. AWS prepared for testing of Xmas tree." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Held TBT with all involved parties prior testing of Xmas tree." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Lined up and tested cement line to KWV w/ 30/345 bar for 5/10 min." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Lined up valves on Xmas tree and filled same with MEG. Pressure tested tree cap connection to 30/345 bar 5/10 min, good test." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Bled pressure and closed SV. Pressure tested SV to 30/345 bar for 5/10 min, good test. Bled off to 42 bar (SIWHP + 5 bar) to closed drain. Opened DHSV and HMV." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Bullheaded 2 m3 MEG into well using MEG injection pump." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Pumped 7,6 m3 of packer fluid with cement unit, 270 - 300 lpm with 320 - 325 bar." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.2 hours. Operational details: Bled down Xmas tree to 45 bar via closed drain. Closed DHSV." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 3.2 hours. Operational details: Inflow tested DHSV for 30 min. Inflow tested HMV for 10 min. Inflow tested MMV for 10 min. Installed 2' weco blind cap on KWV and tested cap to 30/345 bar for 5/10 min. Pressure tested KWV across tree to 30/345 bar for 5/10 min." "On 2013-10-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Disconnected the LCP from DHSV and HMV and re-installed permanent control lines. Well F-1 B handed over to production department at 15:00 hrs. ***Last report on well F-1 B, continued reporting on F-15 C***" "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: *** Note *** Operations on F-15 D P/U 9 5/8' Archer Safelock plug and inspected same." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 633m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: RIH w/ Safelock plug on 5 1/2' DP from surface to 633 m." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 633m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Established circulation and washed the setting area. Installed the 9 5/8' Safelock plug at 633 m as per Archer instructions. Sheared ball valve and closed same. Applied 30 bar on string and opened ball valve, verified pressure drop." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 633m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Lined up and leak tested the Safelock plug to 253 bar/ 10 min from below. Pumped 1897 ltr, bled back same volume. Closed ball valve and released RT." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 633m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Spotted 5 m3 Hivis pill above plug." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: POOH w/ Safelock RT on 5 1/2' DP from 633 m to surface." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: L/D Safelock plug RT as per Archer instructions." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing plug from above." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Lined up and pressure tested Safelock plug to 345 bar/ 10 min from above. Pumped 545 ltr, bled back same volume." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Flushed choke and kill lines. M/U DP stand to TDS and RIH, displaced riser and BOP to SW from 22 m to surface. Drained BOP and riser." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled master bushings. Installed diverter bridle. Informed Production department at 12:45 hrs to shut in production as per SIMOPS procedure." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled diverter. Landed and secured same in setback area." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: N/D and pulled slick joint. Landed same in setback area." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed tension cylinders and N/D BOP. Moved BOP from well centre to test stump." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: N/D and pulled BOP HP riser joint. L/O same. Informed Production department at 16:45 hrs about completed heavy lift operations according to SIMOPS procedure." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Removed split hatches and installed full hatch on F-15 slot." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Prepared cantilever and main deck for skidding." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Performed TBT with all involved personnel prior to skidding operation." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Skidded cantilever from F-15 to F-1 slot." "On 2013-12-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.0 hours. Operational details: Cleared and tidy up after skidding. Not able to install walkways to cantilever due to high wind and no crane weather. Build scaffolding to get access to moon pool from main deck. Meanwhile performed TBT with all involved personnel prior to R/U WL on well F-1B." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Prepared drill floor and removed main hatch on wellhead deck and installed WL hatch." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 4.8 hours. Operational details: WOW. Alternative walkways to moon pool and cantilever was not good enough. No crane weather to install walkways." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 5.5 hours. Operational details: WOW. No crane weather to install walkways." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Installed walkways." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Performed TBT prior to leak test XMT cross." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Prepared to leak test XMT cross." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Leak tested XMT cross to 20 bar for 5 min." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.9 hours. Operational details: Leak tested XMT cross to 120 bar for 10 min. Negative. Had problem getting good high pressure leak test. Opened/closed HMV two times with MMV closed. Opened MMV and leak tested XMT cross to 120 bar for 10 min. Negative. Opened/closed PWV three times. Pumped up XMT cross with max rate up to 160 bar, pressure dropped and stabilized at 120 bar. Leak tested XMT cross to 120 bar for 10 min." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: R/U chiksan on KWV and tested same to 20/345 bar for 5/10 min. Closed LTV and opened KWV and leak tested XMT cross against LTV to 20/160 bar for 5/10 min." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Performed TBT prior to R/U on well." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Removed XMT top cap and installed lower riser and BOP." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: M/U and lifted up upper lubricator and GIH in elevator. Meanwhile lifted perforation gun for run#1 onto HTS (Horisontal transfer system) with rig crane." "On 2013-12-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: M/U and lowered down lower lubricator from rig floor and stabbed lubricator onto BOP. L/D upper lubricator and GIH on rig floor." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Connected hoses to BOP and performed a connection test of lower riser and BOP against swab valve to 120 bar for 5 min." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Performed TBT prior to R/U upper lubricator and GIH." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Connected hoses and stabbed upper lubricator and GIH onto lower lubricator." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Filled lubricator with MEG and leak tested R/U to 20/345 bar for 5/10 min. Bled down pressure. Meanwhile performed TBT prior to P/U BHA#1 perforation gun." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: P/U BHA#1, perforation gun and started to install same in lubricator." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Continued installing BHA#1 into lubricator." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT prior to finalize installation of BHA." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Finalized installation of BHA#1." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Leak tested QTS to 20/345 bar for 5/10 min. Checked valve status on WL rig-up, well and pump units." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Held well contoll drill with WL crew prior to RIH." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.1 hours. Operational details: Opened well and pumped 1500 litres of MEG with AWS pressure test pump. Observed 1,23 bar pressure increase in WHP and no changes on DHPG. Also observed gas in return from lubricator. Concluded that there was a larger volume of gas above DHSV. Decided to use a larger volume pump to pump MEG." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Discussed further action and decided to rig up hose from platform MEG system to kill wing valve." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Closed swab valve. Rigged up hose from platform MEG system to chiksan on kill wing valve. Pumped 1500 litres and equalized/opened DHSV with 88 bar WHP. Also observed pressure increase on DHPG. Filled up and pressured up lubricator to 88 bar. Opened swab valve. Meanwhile lifted perforation guns for run#2 onto HTS (Horisontal transfer system) with rig crane." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3302m. The activity was categorized as 'workover -- perforate' and lasted for 3.2 hours. Operational details: RIH w/ BHA#1, 4,72' OD guns from 0 m to 3302 m MD RKB. Could not pass 3302 m MD RKB." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3276m. The activity was categorized as 'workover -- wire line' and lasted for 1.1 hours. Operational details: Tried several times to pass 3302 m MD RKB, no-go. Max speed 20 m/min. Correlated and positioned guns at firing depth. Perforated between 3264-3276 m MD RKB. WHP dropped from 88 to 85,5 bar. DHPG dropped from 319 to 316 bar. Observed drop in HW." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 550m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: POOH w/ BHA #1, 4,72' OD guns from 3276 to 550 m MD RKB. Observed 300 lbs higher PW." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 550m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: Performed TBT prior to POOH and L/D BHA#1, 4,72' OD guns." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: POOH from 550 m to 0 m. WHP 85 bar." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.6 hours. Operational details: OOH. Closed swab valve and HMV and inflow tested same. Flushed lubricator with nitrogen. Meanwhile lifted perforation gun for run#3 and 4 onto HTS (Horisontal transfer system) with rig crane." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: L/D BHA#1 4,72' OD guns on drill floor and inspected same. All shots fired." "On 2013-12-22, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Checked cable head and prepared BHA#2 4.72' OD guns." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 3.2 hours. Operational details: Checked cable head and prepared BHA#2 4.72' OD guns." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Performed TBT and well controll drill prior to P/U and install BHA#2, 4.72' OD guns into lubricator." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.9 hours. Operational details: P/U BHA#2, 4.72' OD guns and installed same in lubricator." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Leak tested QTS to 20/200 bar for 5/10 min. Checked valve status on WL rig-up, well and pump units. Opened well, WHP 86,5 bar." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 530m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: RIH w/ BHA#2, 4,72' OD guns from 0 m to 530 m MD RKB." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 530m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Powered up logging unit." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3300m. The activity was categorized as 'workover -- perforate' and lasted for 2.4 hours. Operational details: RIH w/ BHA#2, 4,72' OD guns from 530 m to 3300 m MD RKB. Could not pass 3300 m MD RKB." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3251m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Correlated and positioned guns at firing depth. Perforated between 3288-3294 m MD RKB. WHP dropped from 86 to 85,8 bar. Observed drop in HW. Correlated while POOH and positioned guns at firing depth. Perforated between 3245-3251 m MD RKB. WHP increased from 85,8 to 86,5 bar." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: POOH from 3251m to 500 m MD RKB." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Powered down logging unit." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: POOH from 500 m MD RKB to surface." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.2 hours. Operational details: OOH. WHP 87 bar. Closed swab valve and HMV and inflow tested same. Flushed lubricator with nitrogen." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Performed TBT prior to L/D BHA#2, 4.72' OD guns on drill floor." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.1 hours. Operational details: L/D BHA#2 4,72' OD guns on drill floor and inspected same. All shots fired. Found fine sand in recesses on BHA." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: Rebuilt cable head." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT prior to P/U and install BHA#3, 4.72' OD P3 guns into lubricator." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: P/U BHA#3, 4.72' OD P3 guns and installed same in lubricator." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Leak tested QTS to 20/200 bar for 5/10 min. Checked valve status on WL rig-up, well and pump units. Opened well, WHP 89,5 bar." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 530m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: RIH w/ BHA#3, 4,72' OD P3 guns from 0 m to 530 m MD RKB." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 530m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Powered up logging unit." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3270m. The activity was categorized as 'workover -- perforate' and lasted for 2.1 hours. Operational details: RIH w/ BHA#3, 4,72' OD P3 guns from 530 m to 3270 m MD RKB." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3300m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Correlated and RIH and tagged HUD at 3300 m MD." "On 2013-12-23, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3276m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Positioned guns at firing depth. Perforated between 3264-3276 m MD RKB. Got now indications that guns had been fired. Observed no drop in HW. Tried several times to fire guns. Got now indications that guns had been fired." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3300m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: Schlumberger discussed situation with onshore. Picked up and saw an increase in PW of 400 lbs, and also observed pressure changes on pressure trend plot. This indicated that the P3 guns had been fired. RIH and tagged HUD at 3300 m MD RKB." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 550m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: POOH from 3300 m to 550 m MD RKB." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 550m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Powered down logging unit and performed TBT prior to POOH and L/D BHA#3, 4,72' OD P3 guns." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: POOH from 550m MD RKB to surface." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: OOH. WHP 93,5 bar. Closed swab valve and HMV and inflow tested same. Flushed lubricator with nitrogen." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: L/D BHA#3 4,72' OD P3 guns on drill floor and inspected same. All shots fired. Found 3 dl of sand in P3 gun bull nose." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Checked cable head and prepared BHA#4, 4.72' OD P3 guns." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 4.5 hours. Operational details: Continued preparation of BHA#4 4.72' OD P3 guns." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed TBT prior to P/U and install BHA#4, 4.72' OD P3 guns into lubricator." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: P/U BHA#4, 4.72' OD P3 guns and installed same in lubricator." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Leak tested QTS to 20/200 bar for 5/10 min. Checked valve status on WL rig-up, well and pump units. Opened well, WHP 99,5 bar." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 530m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: RIH w/ BHA#4, 4,72' OD P3 guns from 0 m to 530 m MD RKB." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 530m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Powered up logging unit." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3298m. The activity was categorized as 'workover -- perforate' and lasted for 2.2 hours. Operational details: RIH w/ BHA#3, 4,72' OD P3 guns from 530 m to 3298 m MD RKB." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3280m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Tagged at 3298 m MD RKB, correlated depth. Correlated and positioned P3 guns at firing depth. Perforated between 3288-3294 m MD RKB. Observed movement in WHP. Observed drop in HW." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3298m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: Correlated while POOH and positioned P3 guns at firing depth. Perforated between 3245-3251 m MD RKB. WHP increased from 102,2 to 102,3 bar. Observed drop in HW. RIH and tagged 3297,5 m MD RKB, correlated depth." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 550m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: POOH from 3297,5 m to 550 m MD RKB." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 550m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Powered down logging unit." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: POOH from 550m MD RKB to surface." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 3.2 hours. Operational details: OOH. WHP 106 bar. Closed swab valve and HMV and inflow tested same. Flushed lubricator with nitrogen." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: L/D BHA#4 4,72' OD P3 guns on drill floor and inspected same. All shots fired. Found 5 dl of sand in P3 gun bull nose." "On 2013-12-24, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.0 hours. Operational details: Bled down pressure above DHSV from 110 bar to 40 bar. Meanwhile performed TBT prior to R/D WL equipment." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.8 hours. Operational details: Inflow tested DHSV." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: R/D upper lubricator and GIH and laid down same on rig floor. R/D lower lubricator and laid down same on rig floor. Meanwhile bled down pressure above DHSV to 2 bar." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT prior to R/D BOP and lower riser." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: R/D BOP and placed same in moon pool. R/D lower riser and laid down same on rig floor. Installed tree cap." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: R/D chiksan on wellhead." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Finalized R/D of chiksan on wellhead and installed cap on x-mas tree kill wing." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 2.2 hours. Operational details: Prepared for and leak tested x-mas tree cross to 20/200 bar for 5/10 min." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 2.2 hours. Operational details: Leak tested x-mas tree top cap and kill wing cap. 20/345 bar for 5/10 min." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Cleaned hatch deck above well and installed hatch over well." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.7 hours. Operational details: Handed well back to production department. Meanwhile cleaned wellhead and cellar deck area." "On 2013-12-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 9.0 hours. Operational details: WOW prior to skid rig to well F-15D due to too high winds for crane lifting. Meanwhile prepared wireline equipment for demobilization and performed general rig maintenance. Prepared for skidding cantilever. Removed scaffold in moonpool. Pressure tested F-12 contingency manifold and hoses to 20/345 bar for 5/10 min." "On 2013-12-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: WOW prior to skid rig to well F-15D. Wind speed above crane limit. Meanwhile prepared wireline equipment for demobilization and performed general rig maintenance. Prepared for skidding cantilever. Pressure tested F-12 contingency manifold and hoses to 20/345 bar for 5/10 min. Prepared for slip & cut, suspended TDS using derrick work basket." "On 2013-12-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Removed gangway and stairs to cantilever. Held TBT prior to skidding cantilever and performed final checks. Started to skid rig from slot F-1 to slot F-15." "On 2013-12-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.5 hours. Operational details: Finalized skidding of rig from slot F-1 to slot F-15. -------------------------------END OF OPERATION--------------------------------" "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Changed out drum on W/L winch after wind speed dropped below crane limit. Meanwhile serviced TDS and fwd PRS. Took over well F-1 B from production at 11:00 hrs." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Notified production department to shut in wells F-11 and F-12 as per SIMOPS procedure. Meanwhile prepared halfmoon hatches in moonpool." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Received notification of wells beeing shut in at 14:20 hrs. Removed hatch on F-1 slot and installed halfmoon hatches. Meanwhile lifted lubricator to rigfloor." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Transfered operation of HMV and DHSV to AWS local control panel." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for rigging up W/L BOP and riser." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Removed Xmas tree cap. Installed short riser and W/L BOP. Function tested W/L BOP." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT with night shift for R/U wireline riser and lubricator." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.2 hours. Operational details: R/U wireline riser, applied double lift through rotary. M/U riser to W/L BOP. Prepared lubricator and fed cable through same. Lifted lubricator with TDS. Meanwhile SLB built cable head." "On 2014-01-25, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: SLB built and tested W/L toolstring (main and backup) for setting EVO plug." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: SLB built and tested W/L toolstring (main and backup) for setting EVO plug. Lifted tools to rig floor." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT for testing rig up and M/U toolstring." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: M/U dummy toolstring and installed lubricator." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Filled riser with 40% MEG and 60% water using production MEG manifold. Meanwhile lined up cement unit via KWV. Performed line test to 20/345 bar for 5/10 min. Installed bleed line to closed drain." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Pressure tested wireline rig up to 20/345 bar 5/10 min. M/U BHA for run #1 (EVO plug)" "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Drained lubricator using N2. B/O QTS and L/O dummy toolstring. M/U toolstring for run #1 (EVO plug). M/U QTS." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT with day shift for W/L run #1." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Leak tested QTS to 20/345 bar 5/10 min." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Opened HMV and MMV - bled off pressure to 33 bar." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Equalized pressure over DHSV using cement unit, 100 bar - open DHSV. Opened SV." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3290m. The activity was categorized as 'workover -- other' and lasted for 3.2 hours. Operational details: RIH w/ run #1 (EVO plug), 5,72' OD plug from surface to 3290 m." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3147m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Correlated BHA across interval. Set plug at 3147 m." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: POOH from 3147 m to surface. Average pulling speed 21 m/min." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Closed in well as per procedure. Bled off pressure in riser to closed drain, bled down from 87 bar. Purged riser with N2." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Inflow tested SV and HMV." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT prior to laying out toolstring." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Broke lubricator. L/D BHA on deck." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Prepared for W/L run #2 (tubing punch). SLB built cable head and tested toolstring. Meanwhile lined up to test plug with cement unit. Equalized tree cross. Opened HMV. Equalized DHSV with 100 bar, no indication seen. Increased pressure to 200 bar and confirmed DHSV open by volume control." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Prepared for W/L run #2 (tubing punch). SLB built cable head and tested toolstring. Meanwhile bled down pressure from 200 bar to 60 bar using closed drain for low pressure test." "On 2014-01-26, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.2 hours. Operational details: Suspended operations on drill floor and cantilever due to ice falling down. Meanwhile continued pressure bled down for low pressure test." "On 2014-01-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW - ice lumps falling to rigfloor/cantilever due to strong wind. Meanwhile stopped bleed down to closed drain at 40 bar as gas was bled off. Commenced low pressure test of EVO plug 40 bar/5 min." "On 2014-01-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.8 hours. Operational details: WOW - ice lumps falling to rigfloor/cantilever due to strong wind. Meanwhile increased test pressure in steps to 200 bar. Stopped and evaluated situation due to high volume pumped. Discussed options with town regarding test pressure and bled down after pressure test to close drain preventing hydrate formation." "On 2014-01-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW - ice lumps falling to rigfloor/cantilever due to strong wind. Meanwhile pressure tested EVO plug to 225 bar/10 min. Good test." "On 2014-01-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.8 hours. Operational details: WOW - ice lumps falling to rigfloor/cantilever due to strong wind. Meanwhile discussed final test pressure and plan for bled down via F-12 with involved parties on rig and in town. Monitored pressure on F-1 B." "On 2014-01-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: WOW - ice lumps falling to rigfloor/cantilever due to strong wind. Meanwhile held TBT for pressure bleed down. Production department prepared line up to receive bleed from F-1 B. Bled down pressure from F-1 to F-12 from 225 bar to 35 bar." "On 2014-01-27, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.5 hours. Operational details: WOW - ice lumps falling to rigfloor/cantilever due to strong wind. Meanwhile: Monitored WHP on F-1 B. Performed daily maintenance and housekeeping. Bled WHP from 37 bar to 30 bar, using closed drain." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: WOW - ice lumps falling to rigfloor/cantilever due to strong wind. Meanwhile: Monitored F-1 B WHP. Performed daily maintenance and housekeeping." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT for M/U W/L toolstring #2 (tubing punch). Annonced handling of explosives and errected barriers." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Tested and M/U BHA for run #2 (tubing puncher). Leak tested QTS to 20/345 bar 5/10 min." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Filled riser and pressured up same. Opened well as per well entry procedure. WHP 33 bar." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: RIH w/ run #2 (tubing puncher) from surface to 2950 m. WHP 37 bar." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Correlated across perforation interval 2942 - 2945 m. Bled off WHP to 30 bar using closed drain." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2942m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Positioned puncher with top shot at 2942 m. WHP 30 bar/ Annulus pressure 0 bar. Punched interval 2942 - 2945 m." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 160m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH from 2942 m to 160 m. Average pulling speed 23 m/min." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 160m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT for handling explosives and L/O toolstring. Made PA and erected barriers." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: POOH from 160 m into tool catcher." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Closed SV and HMV. WHP 32 bar. Closed DHSV and opened SV. Bled down pressure in riser through closed drain. Closed SV, openend HMV." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Inflow tested SV." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Closed HMV, bled down pressure in XT cross to closed drain." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Inflow tested HMV." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Confirmed guns had been fired. L/O toolstring. Opened DHSV." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Performed TBT for the circulation operation with all involved parties." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Pressure tested surface line up to 20/200 bar 5/10 min." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.8 hours. Operational details: Verified correct line-up. BHP 277 bar, THP 27 bar, AP 0 bar. Established circulation and brought pumprate in steps up to 1200 l/min, with max. open choke (2' choke). Kept BHP constant to 350 bar. Pumped 70 m3 of 1,03 sg packer fluid followed by 10 m3 1,50 sg CaBr brine pill followed by 42 m3 packer fluid, taking returns via F-12 into production." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Stopped pumping and allowed 1,50 sg CaBr brine pill to settle into 7' tubing/liner." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: Pumped 80 m3 1,37 sg OBM w/ 600 - 900 l/min, monitoring downhole pressure and taking returns via F-12. Stopped pumping and routed returns back to choke manifold and pits as requested by production department." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Continued pumping 1, 37 sg OBM w/ 600 l/min. Diverted brine and water returns into dedicated pits. Pumped 100 m3 in total until OBM in returns. MW out 1,30 sg." "On 2014-01-28, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: Circulated B/U to condition mud. Increased rate in steps from 600 l/min to 1200 l/min, pump pressure 70 - 180 bar." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Circulated B/U with 1200 l/min, 180 bar. Conditioned mud until even MW in/out. Circulated in total 4 x B/U. Performed TBT for handling explosives and M/U W/L run #3. Made announcement and erected barriers." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: M/U BHA for run #3 (tubing cutter). Leak tested QTS to 30/345 bar 5/10 min. Opened well as per procedure. WHP 3 bar." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2995m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: RIH w/ run #3 (tubing cutter) from surface to 2995 m. Average running speed 20 m/min." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2948m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Correlated across interval 2995 - 2916 m. Positioned cutter at 2948,5 m. Performed cut." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 120m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: POOH from 2948 m to 120 m. Average pulling speed 19 m/min." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 120m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Performed TBT for handling of explosives and R/D W/L. Erected barriers and made announcement. Informed production department to shut in wells as per SIMOPS." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: POOH into tool catcher. Closed SV." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Closed HMV, opened SV. Drained riser/lubricator with N2. Broke lubricator. Confirmed cutter fired and L/D BHA on deck." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: R/D lubricator and W/L riser." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Attempted to open DHSV. Confirmed closed, unable to circulate. Equlized pressure over DHSV. Confirmed open by circulation." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Inflow tested DHSV 30/200 bar 10 /30 min. 1124 l pumped, 1120 l bled back." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/D wireline BOP and lower riser." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: N/D and lifted W/L BOP and riser off F-1. Meanwhile cleaned and cleared rig floor from W/L equipment." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for installing BPV in tubing hanger" "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Prepared Xmas tree and installed BPV as per Vetco procedure. Meanwhile R/D and packed W/L equipment." "On 2014-01-29, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Rambøll disconnected instrumentation and control lines. Drained flow line. Meanwhile R/D and packed W/L equipment and prepared for B/L." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Removed flow line from F-1 tree. Drained Xmas tree and N/D same. Meanwhile packed W/L equipment and prepared for B/L." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed hatches on slots F-1 and F-6. Removed middle beam. Removed master bushing." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT for lifting tree with TDS." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Removed Xmas tree. Lifted same off F-1 using TDS. Shifted load to overhead crane in moonpool and landed tree on transport skid." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Drained spool piece. Meanwhile installed beam and hatch on slot F-6." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lifted spool piece to rigfloor using TDS. Installed master bushing." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Cut and removed control lines on multibowl. Meanwhile P/U HP riser joint and suspended same with TDS." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered and landed riser joint. M/U same to multibowl." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Installed split hatches and half moons on F-1 slot." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Built scaffold around riser. Meanwhile serviced TDS and travelling block." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Skidded BOP to well center. Meanwhile spotted Weatherford equipment on rig floor." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Prepared to skid rig forward. Meanwhile R/U Weatherford equipment on fwd hydraulics and tested same." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT prior to skidding cantilever." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded cantilever forward to align BOP over riser. Installed stairs and walkways." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT prior to N/U BOP." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Landed BOP. Installed slick joint. Informed production department at 21:15 hrs about completed lifting operations." "On 2014-01-30, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: M/U NT2 connector. Installed BOP tensioners." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed diverter." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: M/U slick joint connection." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: R/D diverter handling equipment. Filled BOP and riser with 1,37 sg OBM." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: R/U 3 1/2' handling equipment. Moved Weatherford equipment to setback area." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed TBT for installing dart in BPV and P/T BOP." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: P/U and M/U BPV dart RT. RIH and installed dart in BPV as per GE Vetco procedure." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Closed blind/shear rams. Pressure tested BOP connector agains BPV to 20/345 bar for 5/10 min." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: POOH and L/O 2 singles 3 1/2' DP and dart RT." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Changed elevator inserts to 5 1/2'. Tidied and cleared rigfloor." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: P/U 5 1/2' DP stand and M/U to 7' x 5 1/2' x-over." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 2.5 hours. Operational details: R/U Weatherford tong and function tested same. Meanwhile installed BHA washer. M/U FOSV to 7' x-over." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed TBT prior to retrieve TH." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: P/U and M/U tubing hanger retrieving tool." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Attempted to M/U TDS to stand, w/o success. Prepared permit and isolated equipment to use derrick work basket. Lowered TDS to floor and investigated. Shaft rotated freely, spin function ok. De-isolated TDS and drawworks." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Run TDS up and latched onto stand. Attempted to spin in TDS, no success. Attempted to unlatch BX elevator w/o success. Troubleshot elevator malfunction." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Evaluated situation and discussed way forward. Held TBT. Removed THRT from string and L/D same. B/O and L/O DP singles from bottom up." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Performed fault finding on elevator open/close function. No success." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed elevators and function tested same." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Function tested spin function on TDS at various levels to aid fault finding." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Isolated equipment, TDS and drawworks. Disconnected and blanked off TDS brake hydraulics. Function tested TDS. Observed same intermittent error on brake system." "On 2014-01-31, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Lowered blocks to lowest possible position to allow maintenance access (wind speed above 60 kts). Isolated equipment, TDS and drawworks. Maintenance department removed TDS cage and striped down TDS brake system for investigation/removal of brake discs." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Maintenance department stripped down TDS brake system for investigation/removal of brake disc." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 7.8 hours. Operational details: Maintenance department removed disc from brake. Re-assembled brake system and installed same on TDS. Meanwhile performed cleaning and housekeeping." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Tested the TDS at various heights in both spin and drill mode. Erratic torque observed but TDS spin function not stopped." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Tested TDS at connection height in derrick. Observed high torque in reverse mode and no turning. Selected forward mode, high torque and no turning. Maintenance engineer and electrician inspected TDS at height. Lowered TDS down. Function tested same, ok. Meanwhile layed out 2 7/8' DP on pipe deck." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: Isolated TDS. Inspected gear box on TDS and replaced gear box filter. Meanwhile performed maintenance and housekeeping. Preserved BOP test stump in moonpool." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Perform TBT and checked TDS for PDOs. Installed TDS cage." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Performed megger testing of the TDS umbilical at various heights, unable to replicate fault." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Isolated equipment. Checked and wire locked bolts on TDS. De-isolated equipment." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Reinstalled link tilt and elevators, tested same." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for running THRT." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U THRT and landed same in rotary. Installed bushings. M/U 5 1/2' DP stand to THRT." "On 2014-02-01, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: RIH w/ THRT on 5 1/2' DP stand from surface to 21 m." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Engaged TH as per GE Vetco instructions. Pulled to 110 t (40t overpull), observed actuating ring release. Continued to pick up, weight dropped of at 140 t hookload. POOH and inspected RT, no damage observed. RIH and engaged TH as per GE Vetco instructions, no clear indication of tool beeing fully engaged. Suspected actuator ring rotating." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up to 140 t, set back weight to 3 t on TH. Re-engaged retrieving tool. Picked up to 190 t hookload (120 t overpull) and pulled TH free." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed flowcheck. Well stable." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH w/ tubing and tubing hanger on THRT and 5 1/2' DP stand from 21 to surface, 170 t up weight. Landed TH in c-plate." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Attempted to break out TDS, observed high torque on motor. Confirmed IBOPs not breaking out. Broke out from stand, 20 - 30 kNm torque." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Released THRT from tubing hanger. Required several attempts to come free. Inspected hanger, observed first quarter of actuator ring shoulder bent upwards. R/B stand and THRT in aft PRS." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed communication collar and BPV from hanger." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT prior to R/U for pulling completion." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: R/U 7' tubing handling equipment and Weatherford power tong." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Installed TH handling tool. P/U string, removed c-plate and master bushings. Installed Weatherford compact spider slips." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed control line and DHPG cable. B/O and L/D tubing hanger." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2926m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with day crew for pulling completion." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2876m. The activity was categorized as 'workover -- completion string' and lasted for 1.8 hours. Operational details: POOH 7' tubing from 2926 m to 2876 m. Removed clamps and spooled control line/DHPG cable on to reel. L/O joints to deck." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2876m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: Changed slip inserts and installed wiper rubber to improve pipe cleaning." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2817m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: POOH and L/O 7' tubing from 2876 m to 2817 m. Removed clamps and spooled control line/DHPG cable. Well not taking correct fluid volume." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2817m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min, well stable." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2736m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: POOH and L/O 7' tubing from 2817 m to 2736 m. Trip tank static while POOH." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2714m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Pulled 2 joints of tubing at controlled speed to monitor displacement. Well taking correct volume." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2576m. The activity was categorized as 'workover -- completion string' and lasted for 2.0 hours. Operational details: POOH and L/O 7' tubing from 2714 m to 2576 m. Removed clamps and spooled control line/cable. Average 6 joints/hr." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2419m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Changed out dies on Weatherford tong." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2419m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: POOH and L/O 7' tubing from 2576 m to 2491 m. Removed clamps and spooled control line/cable. Average 7 joints/hr." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2483m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: POOH to 2483 m. Removed clamps and disconnected control line. B/O and L/O DHSV." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2483m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Maersk technical department performed tests on TDS to identify system fault." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2401m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: POOH and L/O 7' tubing from 2483 m to 2401 m. Removed clamps and spooled DHPG cable. Average 7 joints/hr." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2401m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with night shift. Checked equipment." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2185m. The activity was categorized as 'workover -- completion string' and lasted for 1.8 hours. Operational details: POOH and L/O 7' tubing from 2401 m to 2185 m. Removed clamps and spooled DHPG cable. Average 10,6 joints/hr." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2185m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Changed out dies on Weatherford tong." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2066m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: POOH and L/O 7' tubing from 2185 m to 2066 m. Removed clamps and spooled DHPG cable. Average 10 joints/hr." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2066m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Serviced handling equipment." "On 2014-02-02, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1860m. The activity was categorized as 'workover -- completion string' and lasted for 1.5 hours. Operational details: POOH and L/O 7' tubing from 2066 m to 1860 m. Removed clamps and spooled DHPG cable. Average 11 joints/hr." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1710m. The activity was categorized as 'workover -- completion string' and lasted for 1.2 hours. Operational details: POOH and L/O 7' tubing from 1860 m to 1710 m. Removed clamps and spooled DHPG cable. Average 10 joints/hr." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1710m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Serviced handling equipment." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1108m. The activity was categorized as 'workover -- completion string' and lasted for 5.5 hours. Operational details: POOH and L/O 7' tubing from 1710 m to 1108 m. Removed clamps and spooled DHPG cable. Average 9,5 joints/hr." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1108m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with day crew for POOH completion." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 30m. The activity was categorized as 'workover -- completion string' and lasted for 8.8 hours. Operational details: POOH and L/O 7' tubing from 1108 m to 30 m. Removed clamps and spooled DHPG cable. Average 10 joints/hr." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 30m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Removed clamp and cable from DHPG and L/O same on rigfloor." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: POOH and L/O 7' tubing from 30 m to surface. Covered cut on tubing stub and L/O same." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: Cleaned and cleared rigfloor from clamps and loose items. (Wind speed above crane limit). Meanwhile covered perforations on 7' tubing joint with rags and tape." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 1.8 hours. Operational details: R/D handling equipment and Weatherford slips/tong. Installed master bushing." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Performed TBT with night crew." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- completion string' and lasted for 0.8 hours. Operational details: Re-arranged completion sub assemblies on rigfloor in order to use HTS, unable to lift out due to wind speed speed above crane limit." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: B/O THRT from stand. L/D tool on setback area." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and installed bowl protector to RT. RIH with bowl protector to 21 m and installed same." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with RT and observed bowl protector still attached to tool." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Performed tests on TDS as per Maersk technical department instructions." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH to 21 m and set bowl protector. POOH and L/D RT." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Cleared rigfloor of 7' completion sub-assemblies. Used HTS and PDM as wind speed above crane limit." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT prior to run 2 7/8' cement stinger." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed 2 7/8' air operated center latch elevators. Hydraulic mechanic installed air hose and fittings on TDS for elevators." "On 2014-02-03, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed handling equipment and R/U Weatherford power tong." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Attempted to P/U first 2 7/8' joint from HTS. Unable to tilt and close center latch elevator, bail rotator not designed for this type of elevator. Evaluated different options. Attempted to tilt elevator using tugger. Unable to latch elevator. Discussed situation and decided to go ahead with TDS repair/change out of torque encoder." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Isolated TDS and drawworks." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.8 hours. Operational details: Maersk technical team replaced torque encoder on TDS. De-isolated TDS and drawworks. Tested TDS, same fault occuring." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed BX elevators and changed inserts to 3 1/2'." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Evaluated situation and way forward wrt to next operation. Discussed w/ onshore organisation." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: Decided to repair TDS and prepare for production riser retrieval to meet upcoming weather window. Maersk technical crew continued to test TDS and troubleshot fault." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Held TBT and R/D Weatherford equipment." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 587m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: P/U and RIH w/ 9 5/8' Safelock plug on 5 1/2' DP from surface to 587 m." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 587m. The activity was categorized as 'interruption -- maintain' and lasted for 3.8 hours. Operational details: R/U to change out TDS service loop. Removed service loop covers and isolated equipment. Unspooled new service loop on rig floor." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 587m. The activity was categorized as 'interruption -- maintain' and lasted for 2.8 hours. Operational details: R/U sheave and tugger up in derrick and lifted tools into derrick. Disconnected service loop from monkey board level. Lowered same to rig floor." "On 2014-02-04, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 587m. The activity was categorized as 'interruption -- maintain' and lasted for 5.0 hours. Operational details: Replaced TDS service loop." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 587m. The activity was categorized as 'interruption -- maintain' and lasted for 5.0 hours. Operational details: Replaced TDS service loop. De-isolated equipment and tested TDS functions at different heights as per ET/Siemens instructions. Performed manriding and installed tarpaulin to TDS umbilical hoses. De-isolated TDS." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 620m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: RIH w/ Safelock plug. Established circulation and washed the setting area, 1100 l/min, 14 bar. Installed the 9 5/8' Safelock plug at 619,6 m (center element). Load tested the plug with 20 T down weight. Top of plug at 617 m." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 620m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.5 hours. Operational details: Lined up and pressure tested the surface lines. Pressure tested the Safelock plug from below to 20/232 bar for 5/10 min. Pumped 1851 ltr/bled back 1620 ltr." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 620m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Closed ball valve and released RT from plug as per Archer instructions." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH w/ Safelock RT on 5 1/2' DP from 619 m to 170 m. Meanwhile displaced choke/kill line to seawater and pressure tested line to 300 bar." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Displaced well to SW from 170 m to surface w/ 2400 l/min. Pumped base oil and soap pill as per displacement plan." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH on 5 1/2' DP from 170 m to surface. L/O Archer RT." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Pressure tested the Safelock plug from above to 20/232 bar for 5/ 10 min. Pumped 450 ltr, bled back same volume." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U bowl protector RT. RIH and retrieved bowl protector. L/D same." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U and M/U MS-T seal retrieval tool. Tested tool on surface as per GE Vetco instructions." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH to 21 m. Secured control lines with duct tape." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Engaged MS-T RT and unseated seal as per GE Vetco instructions. Pulled seal assembly free with 76 Mt overpull." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH and removed control lines from string. L/D tool to setback area." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for releasing tension from tieback string using DrilQuip adjustable sub setting tool. Meanwhile drained riser." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 26m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: M/U DrilQuip adjustable sub setting tool and RIH w/ same on 5 1/2' DP stand from surface to 26 m." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 26m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Set adjustable sub tool, applied 100 bar pressure on string, took 22 MT overpull. Removed tension from tieback string as per DQ instructions." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 26m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Attempted to release tool. Observed overpull. Made several attempts to release tool w/o success." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 26m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation and DrilQuip technical support. Decision made to break out tieback adapter and recover same with stuck DQ tool." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 26m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Broke out tieback adapter w/ 3 LH turns, 2-10 kNm. P/U string, observed tieback string free and 5-8 MT additional weight." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: POOH w/ 10 3/4' tieback and stuck adjustable setting tool on 5 1/2' DP stand. B/O double and R/B same in double latch." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 3.0 hours. Operational details: R/U handling equipment for 10 3/4' casing. Changed out Weatherford power tongs. Prepared FMS. Cleared rigfloor and temporary stored tools in setback area (wind speed above crane limit)." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT after crew change." "On 2014-02-05, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Moved Weatherford tong to well center and installed hydraulic hoses." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Installed hydraulic hoses and function tested Weatherford tong." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT for B/U and handling of casing hanger, stuck DQ tool and DP joint in one assembly." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Pulled casing hanger above rotary. Set manual slips on 10 3/4' hanger pup and installed dog collar on 5 1/2' DP above hanger. Continued POOH until 10 3/4' pup joint below adjustable sub at surface. Set slips and dog collar. B/O assembly and parked same at setback using aft PRS." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 120m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Installed 10 3/4' elevator and Weatherford FMS." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.5 hours. Operational details: POOH and L/D 10 3/4' casing joints." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Due to high wind and no crane operation, replanned for storage of equipment on rigfloor. Moved equipment and rigged down casing tong and elevators." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued moving equipment and rigged down casing tong and elevators." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT to discuss plan for nippling down Diverter and BOP." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Rigged up Diverter chains. Removed bushings and BHA washer. Pulled Diverter." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Shut-in production. Disconnected and pulled Overshot." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Removed BOP tensioners. Disconnected NT2. Nippled down BOP. Simultaneously cleared rigfloor of completion equipment and tools." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed diverter chains to surface riser. Removed scaffolding from riser access." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Disconnected multibowl connection. Pulled and layed out riser joint." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Rigged down Diverter chains and installed elevator." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed side outlet valves." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U Tensioning tool to pup joint and stand." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with Tensioning tool and took weight, 115 T upweight." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.5 hours. Operational details: Prepared wellhead and transfered weight from tensioning pistons to block. Disconnected tensioning pistons." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: Rigged down Tension ring assy and removed boat collision stool. Installed nylon protector guide. Removed all protruding nuts and bolts from Multibowl. Meanwhile broke out single of 5 1/2' DP, adjustable sub and XO from 10 3/4' csg assy and L/D same to deck." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT for removing hatches and rigging up for running Guidewires and hotstab on minireel hose." "On 2014-02-06, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Started to remove hatches from slot F-6 and rigging up sheaves in moonpool to run Guidewires and Mini reel" "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued to remove hatches from slot F-6 and rigged up sheaves in moonpool to run Guidewires and Mini reel hose." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Launched ROV and ran Guidewires. Attached same to Eagle clamps. Sat down 15 T on tieback connector. Meanwhile ran Hotstab." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed Dummy Hotstab. Flushed the Hotstab and installed into receptacle at the top of Connector. Manipulated valve to test same." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waiting on crane and supply vessel to clear congested decks and drill floor due poor weather conditions in the past few days. Maenwhile prepare to retreive HP production risers." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.2 hours. Operational details: Waiting on crane and supply vessel to clear congested decks and drill floor due poor weather conditions in the past few days. Meanwhile held TBT and landed BOP on NT2 connector. Isolated TDS. Performed rig floor PMs." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT before disconnecting." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Disconnected PR TBC. Lifted up 20 cm. Removed Hotstab and installed dummy Hotstab." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Lifted Spider to rigfloor. Spotted Well Partner equipment on rigfloor and removed Moonpool hatches." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled riser to rigfloor and racked DP stand." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT for rigging up Spider." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Removed bushings and installed Spider. Rigged up handling equipment. Meanwhile ROV installed debris cap." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Picked up and sat Riser Tension joint in slips. Broke out flange." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on deck to prepare for receiving Risers from drillfloor." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/D Tensioning joint to deck." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Pulled and L/D 1 single and 1 double Production riser. Power washed each fairring." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-02-07, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.8 hours. Operational details: Pulled and L/D remaining Risers from 73 m to RKB. Power washed eached fairing. Covered Spider. Notified Production of end of operation at 23:24 hrs. Cleaned and cleared rigfloor." "On 2014-02-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather. Meanwhile: Isolated system and held TBT for TDS brake disc job." "On 2014-02-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.5 hours. Operational details: Waited on weather. Meanwhile: Performed job on TDS brake disc. Simultaneously ran Riser Guide Funnel and landed same onto Wellhead. Installed debris cap." "On 2014-02-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.5 hours. Operational details: Waited on weather. Meanwhile: Performed job on TDS brake disc. Tested same. Simultaneously M/U BOP NT2 connector. Startet to pressure test BOP to 20/345 bar for 5/10 min. ROV installed VX ring." "On 2014-02-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.5 hours. Operational details: Waited on Weather. Meanwhile continued testing BOP to 20/345 bar for 5/10 min. Performed general PMs and cleaned and cleared in drilling areas." "On 2014-02-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on Weather. Meanwhile held TBT and pulled Hotstab lines from Moonpool to rigfloor. Function tested Drilling Riser Connector. Held TBT and L/D Connector to deck." "On 2014-02-08, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: Waited on Weather. Tested Kelly hose, lower and upper IBOP to 20/345 bar for 5/10 min. Performed general PMs and cleaned and cleared in drilling areas." "On 2014-02-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: Waited on Weather. Meanwhile tested manifolds to 20/345 bar for 5/10 min.. Performed general PMs and cleaned and cleared in drilling areas. Performed service on PRS and TDS." "On 2014-02-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waited on Weather. Meanwhile held TBT and P/U Drilling Riser Connector. Changed out casing tong to 2 7/8'." "On 2014-02-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 15.0 hours. Operational details: Waited on Weather. Meanwhile moved XMT. Performed general maintenance and cleaned and cleared in drilling areas. Assisted deckcrew preparing backload. Pressure tested Choke manifold to 20/345 bar for 5/10 min." "On 2014-02-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on Weather. Meanwhile re-function tested Drilling Riser Connector." "On 2014-02-09, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waited on Weather. Meanwhile performed general maintenance and cleaned and cleared in drilling areas. Continued pressure testing Choke manifold to 20/345 bar for 5/10 min." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on Weather. Meanwhile performed general maintenance and cleaned and cleared in drilling areas. Production shut down at 05:00 hrs." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH with Drilling Riser Connector" "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued RIH with Drilling Riser to 21 m." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 9.5 hours. Operational details: Continued RIH with Drilling Riser from 21 to 103 m. Resumed production according to yellow SIMOPS at 10:30 hrs." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed from BX elevator to 24' csg elevator." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT prior to picking up Tensioning joint." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: P/U Tensioning joint and M/U same." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew" "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Ran Tensioning joint and landed same on C-plate." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed DP elevator and rotator" "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U BOP joint" "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: M/U BOP joint and tested same." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lifted string. Removed casing elevator and C-plate. Removed Riser Spider." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed Outer ring, Master bushing and Bowls." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U XO and landing single." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: ROV removed hole cover from Guide Funnel." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lowered Connector down above Guide Funnel. Re arranged Guide Wire for centralizing." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lowered Connector down into Guide Funnel." "On 2014-02-10, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Recovered Tugger to run lifting bridle for Guide Funnel." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lowered lifting bridle for Guide Funnel to sea floor and attached same to Funnel. Removed Funnel and sat aside." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT with all involved personnel." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Landed Drilling Riser Connector and sat down 20 T. Ran Hot stab. Flushed and installed same. Manipulated TBC panel." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pressured up through Mini reel to 3000 psi for 13 min to lock Connector. Bled down to zero bar." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed 15 T overpull test to verify Connector locked." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: ROV pulled Hot stab and inserted dummy. Recovered Hot stab to rig." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Installed hatches on lower deck prior to filling Riser" "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Build scaffolding to access Claxton tool in Moonpool." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued building scaffolding to access Claxton tool in Moonpool." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Filled riser at 500 LPM / 1 bar." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT before pressure test" "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed low pressure test of Drilling Riser and Connector to 100 bar for 10 min. Bled of pressures." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Held TBT. Discussed method and hazards for installing Centralizers and Tensioning system." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 5.5 hours. Operational details: Installed Centralizers and Tensioning system." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Applied 20 T tension on each Tensioner. Released weight on TDS. Disconnected TDS." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Released Claxton ring." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Broke down XO and L/D single and Claxton tool." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Rebuild scaffolding in Moonpool for access to NT2." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT for nippling BOP." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Transported BOP from setback to riser. Rigged up Diverter chain." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT prior to installing slick joint and Diverter." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed Master bushing and Outer ring." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Run and landed slick joint and Diverter. Informed Production at 19:57." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: M/U all connections and installed BOP tensioning system." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Filled BOP with seawater." "On 2014-02-11, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Confirmed lineup and performed linetest. Performed Connector test to 20/232 bar against Safelock plug and Shear Ram for 5/10 min. Bled off pressure. Simultaneously pulled Guide Funnel to rig." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed PS21 slips." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 8m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: M/U Safe Lock retrieving tool and checked same." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with Safe Lock retrieving tool on 5 1/2' DP to 170 m." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Displaced manifolds, U-tube and Kill and Choke lines to 1,37 SG OBM." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Displaced well from 170 m to 1,37 SG OBM with 2500 LPM/12 bar." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 605m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH with Safe Lock retrieving tool on 5 1/2' DP to from 170 to 605 m." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 605m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Established circulation with 300 LPM / 10 bar. Recorded up/down weights: 87/84 T. Rotational weight 85 T / 2 kNm." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 605m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT prior to pulling plug with focus on well control." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 605m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Trouble shoot BOP UPS failure alarm." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 617m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Established circulation and RIH to above plug. Attempted to latch onto plug putting down 15 T - No Go." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 617m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Applied 3 RPM and latched onto plug. Applied 30 bar pressure on DP before opening plug. Confirmed latch with 10 T overpull. Waited 10 min for plug element to retract." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 617m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 8m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: POOH from 617 to 8 m with safe Plug on 5 1/2' DP. Restricted pulling speed of 30 m/min." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Inspected Safe Lock assy and L/D same." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: M/U cement side entry assy." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT for rigging up equipment." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Rigged up 2 7/8' tubing handling equipment. Changed out elevator inserts to 2 7/8'." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: TOFS: Prepared SJA and discussed use of manual 2 7/8' slips." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: TOFS: Performed derrick and TDS drop inspection." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 9m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: P/U and M/U Mule shoe. P/U one 2 7/8' tubing joint. Attempted various means of stabbing remotely - no go." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 9m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Rigged up tong tailing arm. Function tested same." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 27m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U second and third 2 7/8' tubing joints from deck and fine tuned stabbing arm. RIH to 27 m." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 27m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew (short change)." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.2 hours. Operational details: RIH with 2 7/8' tubing cement stinger from 27 to 350 m." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Changed dies in casing tong. Broke down well control assy. M/U XO with casing tong." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Rigged down casing tong." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U XO assy from 2 7/8' to 5 1/2' DP." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed master bushing and installed PS21." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1726m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: RIH with cement stinger on 5 1/2' DP from 350 to 1726 m. Speed restricted due to high wind." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1726m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Fitted rope around dog house window guard to avoid hoses catching under." "On 2014-02-12, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2735m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: RIH with cement stinger on 5 1/2' DP from 350 to 1726 m." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3097m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Continued RIH with cement stinger on 5 1/2' DP from 1726 to 3097 m." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3097m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Staged up pumps to 500 LPM / 55 bar." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3148m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Washed down slowly with 500 LPM/55 bar and tagged EVO plug at 3148 m. Tagged twice with 1-2 T on plug." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3140m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.2 hours. Operational details: Conditioned mud until even MW in/out. Circulated 3 1/2 btm up. Started with 1710 LPM/275 bar due to high pump pressure and went slowly up to 2100 LPM/270 bar as the mud became conditioned." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3140m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT for cement job." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3144m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Racked back last stand and M/U 6 m pupjoint and cement assy. RIH to 3144 m. Installed cement hose. Applied 20 bar. Confirmed line-up." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3144m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Pumped 8 m3 1,60 SG spacer with rig pump. Changed lineup to cement unit. Applied 30 bar behind IBOP. Waited for crewchange." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3144m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT for all involved in cement job." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3144m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Mixed and pumped 8,3 m3 1,90 SG GasStop cement." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3144m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed cement hose and lined up from rig pumps." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3144m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pumped additional 1,8 m3 1,60 SG spacer using rig pumps. Displaced cement with 1,37 SG OBM using rig pumps. Displaced at 2200 LPM/280 bar and 30 RPM/8 kNm." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 3140m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Broke out and L/D cement assy." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2750m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: POOH with cement stinger on 5 1/2' DP from 3140 to 2750 m. Restricted pulling speed: 3 min/stand. No wet pipe seen." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2750m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Installed 2 x wiper balls and circulated btms up with 2300 LPM/265 bar and 40 RPM/6 kNm. No cement, but spacer in return." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2490m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH cement stinger on 5 1/2' DP from 2750 to 2490 m." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2490m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Performed kick drill while flowchecking well on triptank for 15 min. Well static. Pumped 3 m3 slug and chased same." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1800m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH cement stinger on 5 1/2' DP from 2490 to 1800 m. Damage to slips occured." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1800m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Pulled, cleaned, greased and inspected PS21 due to damage." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1200m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH cement stinger on 5 1/2' DP from 1800 to 1200 m. PRS encoder problems occured." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1300m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed from aft PRS to forward PRS due to encoder problem." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 360m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: POOH cement stinger on 5 1/2' DP from 1200 to 360 m." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 360m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed PS21 and installed Master bushing." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 360m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Broke out X/O and racked back last stand of 5 1/2'" "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 360m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT for rigging up casing tong." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 360m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Rigged up casing tong." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 360m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U well contingency sub. Cleaned and cleared on rig floor before manual handling." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 150m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: POOH with 2 7/8' cement stinger from 360 to 150 m and L/D same to deck." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 150m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 110m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Continued POOH with 2 7/8' cement stinger from 150 to 110 m and L/D same to deck. Fitting on elevator broke." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 110m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Repaired leaking hydraulic fitting on BX elevator." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Continued POOH with 2 7/8' cement stinger and Bull nose from 110 m to surface and L/D same to deck." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT for rigging down casing tong." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Rigged down casing tong." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: P/U Clean-out assy from deck. Checked same." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held TBT for changing handling equipment and RIH with BHA." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed handling equipment." "On 2014-02-13, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 168m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with Clean-out assy on 5 1/2' HWDP to 168 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 168m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Removed Master bushing and installed PS21 slips." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 980m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.2 hours. Operational details: RIH with 8 1/2' Clean-out assy on 5 1/2' DP from 168 to 980 m. Noticed incorrect return volume." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 980m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: When filling pipe it was concluded that float didn't work. Established circulation and attempted to close float with 980 LPM." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1124m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued RIH with 8 1/2' Clean-out assy on 5 1/2' DP from 980 to 1124 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1165m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Checked string. Float not working. Established circulation and attempted to close float with 2500 LPM. RIH one stand and checked float. Still not working." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2030m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.5 hours. Operational details: Continued RIH with 8 1/2' Clean-out assy on 5 1/2' DP from 1165 to 2030 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2030m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation with 1240 LPM/48 bar to verify unplugged string." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2188m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Continued RIH with 8 1/2' Clean-out assy on 5 1/2' DP from 2030 to 2188 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2188m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed kick drill. Stabbed FOSV and closed same in 55 sec." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2309m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued RIH with 8 1/2' Clean-out assy on 5 1/2' DP from 2188 to 2309 m. Pipe slipped out in derrick." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2309m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Stopped and performed TBT and SJA before recovering pipe from derrick. Prepared equipment." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2309m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Held TBT and SJA. Prepared equipment." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2309m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Recovered dropped pipe stand from derrick. Inspected all contact areas." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2712m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.0 hours. Operational details: Continued RIH with 8 1/2' Clean-out assy on 5 1/2' DP from 2309 to 2712 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2712m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: M/U TDS and performed measurements: Up/down weight: 154/131 T. Rotational weight 141 T / 8-10 kNm. 1000 LPM/35 bar." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2878m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.2 hours. Operational details: Reamed down from 2712 to 2878 m with 2000 LPM/110 bar and 60 RPM/8-15 kNm. Dry cement cuttings on shakers." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2878m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Tagged hard cement at 2878 m with 10 T. Confirmed tagging." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2870m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.0 hours. Operational details: Racked back one stand and circulated btm up with 3000 LPM/229 bar and 20 RPM/7-8 kNm." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 2870m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flowchecked well on TT - well static." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.8 hours. Operational details: POOH with 8 1/2' Clean-out assy on 5 1/2' DP from 2870 to 1457 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 3.0 hours. Operational details: M/U TDS and circulated to reduce MW from 1,38 to 1,28 SG. Filled sand traps to assist with centrifuge. Simultaneously broke out and L/D cement assy. Changed out casing tongs." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pumped slug and chased same." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 977m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.8 hours. Operational details: POOH with 8 1/2' Clean-out assy on 5 1/2' DP from 1457 to 977 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 977m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 210m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.8 hours. Operational details: POOH with 8 1/2' Clean-out assy on 5 1/2' DP from 977 to 210 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 7m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: POOH with 8 1/2' Clean-out assy on 5 1/2' HWDP from 210 to 7 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 7m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held TBT for removing PS21 slips and handling BHA." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 7m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed Master bushing." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: L/D 8 1/2' Clean-out assy to deck." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Held TBT for handling Cutting assy. Cleaned and cleared rig floor." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: P/U 9 5/8' Cutting assy. Connected TDS and tested knives. Prepared knives for RIH." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Installed PS21 slips." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 214m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH with 9 5/8' Cutting assy on 5 1/2' HWDP from 10 to 214 m." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 534m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: Continued RIH with 9 5/8' Cutting assy on 5 1/2' DP from 214 to 534 m. Filled pipe at 494 m. Leakage on forward PRS hydraulic hose occured." "On 2014-02-14, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 534m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Repaired leaking hose on forward PRS." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 534m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Continued repairing leaking hose on PRS." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 815m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Continued RIH with 9 5/8' Cutting assy on 5 1/2' DP from 534 to 815 m." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 815m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.8 hours. Operational details: Waited on Weather due to wind above the 65 knots limitation of PRS. Monitored well on Trip Tank." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Continued RIH with 9 5/8' Cutting assy on 5 1/2' DP from 815 to 1422 m." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Connected TDS and filled pipe. RIH to below 1457 m and recorded parametres: Up/down weights: 120/109 T. 800 LPM/44 bar. Positioned pipe at 1457 m and cut 9 5/8' casing according to procedure. Verified cut by sound, pressure and torque. Continued cutting for 5 min." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Pumped slug. Chased same." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 215m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: POOH with 9 5/8' casing Cutter assy on 5 1/2' DP from 1457 to 215 m. Speed restricted due to Cutters in string." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH with 9 5/8' casing Cutter assy on 5 1/2' HWDP from 215 to 10 m. Speed restricted due to Cutters in string." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed Master bushing." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned, inspected and L/D Cutter assy to deck." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U Jetting sub, one stand of 5 1/2' HWDP and Lock Down Retrieval tool. RIH to 50 m." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with Lock Down Retrieval tool from 50 to 138 m on 5 1/2' DP. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Jet washed with 3000 LPM/52 bar. Made 5 passes." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued RIH with Lock Down Retriveval tool from 138 to 190 m bit depth. J'ed into sub as per instructions." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with Lock Down Retrieval tool on 5 1/2' DP from 190 to 50 m. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled and checked Lock Down Retrieval tool. No Lock Down assy attached. Re-sat tool. Misrun." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with Lock Down Retriveval tool from 50 to 190 m. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: J'ed into sub as per instructions." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with Lock Down Retrieval tool on 5 1/2' DP from 190 to 50 m. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled and checked Lock Down Retrieval tool. No Lock Down assy attached. Re-sat tool. Closed piston fully." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with Lock Down Retriveval tool from 50 to 190 m. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: J'ed into sub as per instructions. Pulled with 20 T over pull and observed." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with Lock Down Retrieval tool on 5 1/2' DP from 190 to 50 m. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled and checked Lock Down Retrieval tool. Lock Down assy attached." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Released Lock Down sub from retrieval tool." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: M/U Retrieval tool to string. Observed oil leaked from tool. Trouble shot same. Fumed on rig floor occured." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Cleared rig floor due to fumes from boat alongside." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Filled retrieval tool with oil and resat same." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with retrieval tool on 5 1/2' DP from 50 to 170 m. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Jet washed profile with 3000 LPM/54 bar." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 170m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U stand of 5 1/2' DP and recorded up/down weights: 82/79 T" "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Placed Retrieval tool at 137 m and function tested BOP." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Closed annular with 500 psi and performed friction test up/down: 84 /76 T." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Landed out Retrieval tool on 10 3/4' Seal assy and pulled free with 12 T over pull." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Observed for pressure build up on choke. Pressure stable. Opened BOP." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 50m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with Lock Down Retrieval tool on 5 1/2' DP from 190 to 50 m. Speed restricted." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled Retrieval tool. Removed Seal assy. Re-sat tool and L/D same to deck." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Racked stand of 5 1/2' HWDP and L/D Bull nose." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Installed BHA washer on top of Diverter." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT for P/U Spear assy." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: P/U Spear assy. Inspected and prepared same." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: RIH on 5 1/2' HWDP to 38 m. L/O top single." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Continued RIH on 5 1/2' HWDP from 38 to 119 m." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed kick drill. Stabbed FOSV and closed same in 55 sec." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT for slip and cut drill line." "On 2014-02-15, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Slip and cut drill line." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 119m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Finalized slip and cut." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 144m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: M/U stand of 5 1/2' HWDP to string and connected TDS." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed TBT. Recorded up/down weight: 81/78 T." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1452m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Established 200 LPM/10 bar. Engaged spear at 144 m. Pressure increased to 17 bar. Stopped flow and bled off pressure. Pulled casing free with 174 T on weight indicator. Pulled 10 3/4' x 9 5/8' casing from cut at 1457 to 1452 m. New depth including casing string." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1452m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 3.2 hours. Operational details: Established circulation and took up mud weight from 1,28 to 1,40 SG. Circulated with 2000 LPM/53 bar." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1452m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min - well static." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1452m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Pumped 1,8 SG slug." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: POOH with 10 3/4' x 9 5/8' casing on 5 1/2' HWDP from 1452 to 1314 m." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Released Spear and racked same in derrick." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Started to rig up handling equipment for 10 3/4' casing." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held prejob meeting with ongoing crew regarding rig up of handling equipment." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: Rigged up handling equipment for 10 3/4' casing. Problems with tong occured." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Troubleshot issues with Power Slips hydraulic fittings." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Trouble shot issues with casing door function. Changed out tong. Coupling between Tong and IRN failed." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Coupling between Tong and IRN failed. Fixed same." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Moved spare casing tong from Aux side. Blew a gasket in the roughneck coupling / hose when unmounting tong from frame. Fault on PRS occured." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: VFD fault on forward PRS. Fixed same," "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Installed new casing tong into position." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1314m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT prior to start pulling 10 3/4' casing." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1210m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: Pulled 10 3/4' casing joints from 1314 to 1210 m." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1210m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Rigged up control panel for stabbing arm on tong due to arm slipping forward." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 950m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 3.8 hours. Operational details: Continued pulling 10 3/4' casing joints from 1210 to 950 m. Pulled 6 jnts/hr in average." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 950m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Continued pulling 10 3/4' casing joints from 950 to 850 m." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT for changing handling equipment to 9 5/8'." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Removed Flushed Mounted Spider and Master bushing ring. Installed PS21 with 9 5/8' inserts. Changed lower jaws on casing tong." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: B/O and L/D 10 3/4' x 9 5/8' XO." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Removed elevator and rotator for 10 3/4' and installed BX elevator dressed for 9 5/8'. Changed upper jaws on casing tong. Changed Swedge to 9 5/8'." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 850m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Troubleshot problems with casing tong. Not able to run in automatic mode." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 816m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Pulled 9 5/8' casing from 850 to 816 m. Worked casing tong on tong panel while re-starting tong PLC." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 816m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Worked on sensors on casing tong and calibrated same." "On 2014-02-16, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 721m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Pulled 9 5/8' casing joints from 816 to 721 m." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 19m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 6.0 hours. Operational details: Continued POOH with 9 5/8' casing from 721 to 19 m. Pulled 9,5 jnts/hr in average." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Pulled remaining 9 5/8' and L/D to deck." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT for rigging down handling equipment." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Started to rig down casing handling equipment." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew for rigging down/up handling equipment." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Rigged down casing handling equipment and rigged up for handling DP." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Cleaned and cleared Rig Floor." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT for setting Wear Bushing." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U Jet sub, one stand of 5 1/2' HWDP and WB RT with 13 3/8' WB. RIH to 47 m." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH with Jet sub and WB RT on 5 1/2' HWDP from 47 to 140 m. Speed restricted due to full bore tool." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Jet washed WH with 3000 LPM/58 bar." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 185m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U landing stand and landed 13 3/8' Wear Bushing in profile." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with Jet sub and WB RT from 185 to 47 m. Speed restricted due to full bore tool." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Re-sat WB RT in rotary and L/D same." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Racked stand of 5 1/2' HWDP and L/D Jet sub." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared Rig Floor." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D 10 3/4' Spear assy to deck." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Held TBT for RIH with casing cutter assy." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U 13 3/8' Cutter assy." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Connected TDS and tested cutter with 435 LPM/1 bar." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed Master bushing and installed PS21 slips." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1375m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.8 hours. Operational details: RIH with 13 3/8' casing Cutter assy on 5 1/2' DP to 1375 m. Filled every 500 m without being connected." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1375m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Recorded parametres: Up/down weights: 115/107 T, rotational weight: 110 T, free torque: 4 kNm." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Spaced out to position cutters at 1399 m. Cut 13 3/8' casing with 1000 LPM and 80 RPM." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Flowchecked well on Trip Tank - well static. Pumped 1,8 SG slug and chased same." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 242m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH with 13 3/8' Casing Cutter on 5 1/2' DP from 1399 to 242 m." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 242m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Inspected and performed service on TDS and PRS." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Continued to POOH with 13 3/8' Casing Cutter on 5 1/2' DP from 242 to 10 m." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed PS21 slips and installed Master Bushing." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Pulled 13 3/8' Casing Cutter. Cleaned and inspected same. Racked back in derrick." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared Rig Floor." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U Jet sub, 5 1/2' HWDP stand and WB RT and RIH on 5 1/2' HWDP to 132 m." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Connected TDS and washed WH area with 2500 LPM/40 bar. Disconnected TDS." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 185m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U landing stand and connected TDS. Recorded parametres: Up/down weights: 83/79 T. Engaged Wear Bushing with 5 T. Released WB with 37 T over pull." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with Jet sub and WB RT from 185 to 47 m. Speed restricted due to full bore tool." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released WB from WB RT." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Re-sat tool and L/O WB RT." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U Seal assy RT and inspected same." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT for RIH with Seal assy RT." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH with Jet sub and Seal assy RT on 5 1/2' HWDP from 47 to 132 m." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Connected TDS and washed WH area with 2500 LPM/40 bar. Disconnected TDS." "On 2014-02-17, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 174m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U landing stand and connected TDS. Recorded parametres: Up/down weights: 83/79 T. Closed Annular and recorded parametres: Up/down weights: 85/78 T." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 174m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Opened Annular. Short TBT for landing and dis-engaging Seal assy. Landed off on seal assy. Closed Annular with 600 psi." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 185m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released Seal assy as per procedure. Monitored for pressure build up on choke gauge. No pressure seen. Opened choke fully and opened Annular." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with Jet sub and Seal assy RT with Seal assy on 5 1/2' HWDP. Restricted speed." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 47m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed Seal assy from retrieving tool. Re-dressed Seal assy RT. L/D same." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Racked back stand and L/D Jet Sub." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared Rig Floor. Low level on TDS gear box oil." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Observed low level on TDS gear box. Refilled oil." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT" "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: P/U and L/D 13 3/8' Cutter assy." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: P/U 13 3/8' Spear assy. Inspected and prepared same." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: RIH with Spear assy on 5 1/2' HWDP to 119 m. Up/down weights: 81/78 T" "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Engaged Spear at 140 m. Pulled 13 3/8' casing free with 190 T on weight indicator." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1370m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Pumped 1,8 SG slug. Started to POOH to 1370 m with 13 3/8' Spear and casing on 5 1/2' HWDP." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1259m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Continued POOH with 13 3/8' Spear and casing on 5 1/2' HWDP to Spear/casing at surface." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1259m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Attempted to release Spear. No go. M/U TDS to stand and B/O Spear with 2 rpm/5 kNm. Spear free." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1259m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT for rigging up" "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1259m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: Rigged up casing handling equipment for 13 3/8' casing." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 5m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 9.8 hours. Operational details: B/O and L/D 13 3/8' casing Hanger pup. POOH with 13 3/8' casing joints from 1259 m to 5 m. Pulled 9,4 joints/hr in average." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: L/D 13 3/8' joint with cut. Prepared for rigging down casing handling equipment." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT with ongoing crew for rigging down casing handling equipment." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.2 hours. Operational details: Rigged down casing handling equipment." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Cleaned and cleared Rig Floor." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Held TBT for L/D Spear assy" "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: L/O Spear assy from setback." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held TBT for running Nominal Bore Protector" "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U Jet sub, stand of 5 1/2' HWDP and NBP RT. Installed 20' Nominal Bore Protector on RT." "On 2014-02-18, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH on 5 1/2' HWDP with Jet sub and NBP RT to 132 m. Connected TDS." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flushed WH area with 2250 LPM/34 bar at 140 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Disconnected TDS. M/U landing stand and connected TDS." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 185m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Recorded up/down weights: 82/79 T. RIH slowly with nominal bore protector to setting area." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 185m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed 20' nominal bore protector in profile as per procedure. Disconnected TDS. Racked back landing string." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with Jet sub and NBT RT from 132 to 45 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 45m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed bushings. Re sat NBP RT. Installed bushings. L/D running tool to deck." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Racked remaining stand of 5 1/2' HWDP and L/D Jet sub." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared Rig Floor." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held TBT for RIH with cmt stinger." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 6m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U and M/U cement stinger assy." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 133m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: RIH with cement stinger on 5 1/2' DP from 5 to 133 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 133m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Installed PS21 slips. Tested same." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1348m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Continued RIH with cement stinger on 5 1/2' DP from 133 to 1348 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U TDS and broke circulation with 500 lpm, 4 bar at 1350 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Washed down from 1350 m to 1457 m with 500 lpm, 4 bar." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.5 hours. Operational details: Circulated and conditioned mud with 3000 lpm, 54 bar, 80 rpm, 2-5 kNm prior to conduct cement job. Totally volume pumped 577 m3. Performed pre-job meeting with crew prior to cement job. Weighted up spacer to 1,6 SG." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1457m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pumped 6,6 m3 of hi-vis pill and displaced same with 16,55 m3, 1,5 SG OBM at 1500 lpm, 5 bar." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH from 1457 m to 1399 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: R/U cement assembly and confirmed correct line up with 20 bar." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1399m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Balanced cement plug from 1399 m to 1298 m. Pumped 21,4 m3 of 1,6 SG spacer with 800 lpm, 3 bar. Trapped 30 bar behind IBOP. Mixed and pumped 22,8 m3 of 2,0 SG cement slurry with X 630 lpm, 18 bar. Displaced the cement to the rig floor with 890 l of drill water. Disconnected cement hose and installed bling cab. Zeroed volume counters. Pumped 1,4 m3 of 1,6 SG spacer. Displaced the cement with 12,7 m3 583 strokes of mud with 3000 lpm, 26 bar at 30 rpm, 3-7 kNm. Pulled out of cement to 1220 m. TOC 1298 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1220m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pulled out of cement from 1399 m to 1220 m. TOC 1298 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1220m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 3.2 hours. Operational details: stabed 2 sponge balls in string. Circulated btm's up and string clean with 3000 lpm, 45 bar, 50 rpm, 3-5 kNm. Received 75 m3 contaminated mud/spacer to slop." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1220m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Well static." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1220m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 2 m3 of 1.8 SG slug." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 18m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: POOH with cement stinger from 1220 m to 18 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 18m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed PS-21 slips from rotary. Simultaneously function tested BOP." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: R/B stand. L/O mule shoe and X-O." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: B/D cement assembly and L/O same." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor for excess equipment." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC. Performed pre-job meeting prior to M/U 17 1/2' drilling assembly." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 23m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: WOC. M/U 17 1/2' drilling assembly to 23 m." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 15m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: WOC. Pulled back to 15 m. Plugged into MWD and uploaded MWD." "On 2014-02-19, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 62m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC. M/U 17 1/2' drilling assembly to 62 m." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 109m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: WOC. M/U 17 1/2' drilling assembly to 109 m." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 109m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC. Removed master bushing and installed auto slips in rotary." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 231m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC. Continued to M/U 17 1/2' drilling assembly to 231 m." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1200m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: WOC. RIH 17 1/2' drilling assembly on 5 1/2' DP from 231 m to 1200 m. Filled string @ 700 and 1200 m." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1200m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: WOC. Prepared to P/U and M/U casing. Changed damaged hose on PRS." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1270m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: WOC. Started to wash down from 1200 m to 1270 m with 2000 lpm, 66 bar." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1293m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: WOC. Continued to wash down from 1270 m with 2000 lpm, 66 bar, tagged cement at 1293 m with 6 ton." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1302m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: WOC. Drill/clean out soft cement from 1293 m to 1302 m with 3500 lpm, 198 bar, 60 rpm, 4-7 kNm." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1302m. The activity was categorized as 'interruption -- wait' and lasted for 2.2 hours. Operational details: WOC. Circulated btm's up and clean. Started to wait on cement." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1282m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC. B/O TDS and R/B stand to 1282 m." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1282m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: WOC. Flow checked well for 30 min. Well static." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1282m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: WOC. Closed BOP. Monitored well on choke gauge and trip tank. M/U 13 3/8' casing and set same back in derrick. Replaced BOP control system PSVs." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1282m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: WOW. Monitored well on choke gauge and trip tank. M/U 13 3/8' casing and set same back in derrick. Replaced BOP control system PSVs." "On 2014-02-20, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1282m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: WOW. Opened BOP. Monitored well on trip tank. M/U 13 3/8' casing and set same back in derrick. Performed choke drill with crew. Builded and racked 22 stands of 13 3/8' casing in derrick. Performed inventery on work aloft locker. Checked oil level on TDS gearbox. Changed dies on forw PRS. Rem Hrist alongside at 21:00 hrs, 4,5 m waves." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1282m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: WOW. Monitored well on trip tank. M/U 13 3/8' casing and set same back in derrick." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1282m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Rem Hrist alongside taking on board skips. M/U TDS and established circulation with 1000 lpm, 17 bar. Stopped pumping while skips are placed at swaco unit." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1293m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Established circulation with 3500 lpm, 193 bar. Washed down from 1282 m to 1293 m. Tagged cement with 5 ton." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1340m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Drill/clean out cement from 1293 m to 1340 m with 3500 lpm, 198 bar, 60 rpm, 4-6 kNm, 3 ton WOB, ROP 15 m/hr." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1348m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Drill/clean out cement from 1340 m to 1348 m with 3500 lpm, 193 bar, 60 rpm, 4-6 kNm, 2-3 ton WOB, ROP 15 m/hr." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1351m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Drill/clean out rat hole from 1348 m to 1351 m with 3750 lpm, 209 bar, 60 rpm, 7-12 kNm, 5-7 ton WOB. Drilled in steps of 1 m, pulled into 20' shoe each time." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1355m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Drill/clean out rat hole from 1348 m to 1351 m with 3750 lpm, 210 bar, 60 rpm, 4-6 kNm, 5-9 ton WOB. Drilled in steps of 1 m, pulled into 20' shoe each time." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1355m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Reamed from 1355 m to 1320 m two times with 3750 lpm, 210 bar." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1355m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.5 hours. Operational details: Pumped 5 m3 hi-vis pill and swept hole with same with 2750 lpm, 206 bar." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1355m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Washed from 1320 m to 1355 m with 500 lpm, 2 bar." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1355m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Took SCR @ 1345 m, MW 1,4 SG." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1355m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Recorded up/down and rotating weights, 130/118 ton, 121 ton. Sent down link to autotrak." "On 2014-02-21, at Well NO 15/9-F-1 B, a drilling event occurred at a depth of 1364m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: Commenced time drilling from 1355 m to 1364 m with 3000 lpm,138 bar, 80 rpm, 2-12 kNm, 2-3 WOB. ECD 1,44 SG, ROP 1-3 m/hr. At 14:30 hrs, 50% formation obtained at 1364 MD Operation completed continued operation on 15/9 F-1 C." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 8m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Performed toolbox. Removed hatches and fenced off all levels in WH module. Picked up and hung off 36' hole opener." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Made up powerpulse and drilcollar. RIH with 36' hole opener from 8 m to 50 m MD. Observed leakage on elevator." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Changed leaking fitting on DP elevator." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: RIH with 36' holeopener BHA from 50 m to 140 m MD." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 144m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Stabbed 36' hole opener BHA into F-9 funnel assisted by ROV." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Started washing and rotation with 900 lpm / 40 rpm. Tagged seabed at 144,3 m MD with 5 MT WOB. Washed and rotated down to 150 m MD with reduced parameters : Flow 900 lpm / Rotation 40 rpm / WOB 0,3 MT / Torque 6-14 kNm. ROV observed drill guide bushing landing in guide funnel." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 36' hole section from 150 m to 165 m MD. Drilling parameters : Flow 2700 lpm / Rotation 70 rpm / WOB 2 MT / Torque 12-25 kNm. Performed survey, inclination 1,12 deg." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Reamed drilled section in order to redcue inclination. Observed excessive rattling in drillstring between 159 m and 161 m MD. Performed survey, inclination 0,56 deg. Observed hydraulic leak on TDS." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 165m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Repaired leaking fitting on TDS. Meanwhile pumped 10 m3 hi-vis." "On 2007-11-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 210m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: Drilled 36' hole section from 165 m to 210 m MD. Drilling parameters : Flow 2700-4400 lpm / SPP 70 bar / Rotation 90 rpm / WOB 2-3 MT / Torque 5-14 kNm. Performed survey every 10 m drilled. Swept hole with 20 m3 hi-vis before connections." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 36' hole section from 210 m to 17 1/2' TD at 226 m MD. 36' hole section TD 223 m MD. Drilling parameters : Flow 4400 lpm / SPP 72 bar / Rotation 90 rpm / WOB 0-3 MT / Torque 2-9 kNm. Performed survey every 10 m drilled. Final survey at 226 m MD 0,44 deg." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated 1,5 times bottoms up while reaming hole with 10 rpm. Swept hole with 25 m3 hi-vis at 4400 lpm. Displaced hole from seawater to 80 m3 1,40 sg WBM pumping at 4400 lpm." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 151m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH wirh 36' hole opener BHA from 226 m to 151 m MD. Meanwhile got ROV in position to observe BHA. Topped up hole with 10 m3 1,40 WBM." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 123m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pulled 36' hole opener BHA through funnel while observing with ROV. Observed 8 MT overpull when 36' bit section was pulled through the guide funnel." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 123m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Performed FG check of derrick and TDS. Meanwhile troubleshot standjump function on TDS." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Checked dies on PRS for handling BHA. Continued to POOH with 36' hole opener BHA from 123 m to 50 m MD. Racked back drillcollars in derrick." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Racked back drillcollars in derrick." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to racking MWD and laying out 36' holeopener." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Broke out and racked back stand of DC/powerpulse MWD. Laid out 36' x26' x 17 1/2' holeopener on deck. Cleared and tidied drillfloor." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging conductor running equipment." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Removed elevator and drilling bails. Installed conductor bails and elevator. Transferred slips, bowl and dogcollars to drillfloor." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Took timeout with crews to go through lessons learnt from recent conductor running incident onboard and West Epsilon incident." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to running 30' conductor." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 6m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up shoe joint. Had problems latching elevator due to weldings on joint. Installed casing inserts in RT." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 68m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Ran 30' conductor from surface to 68 m MD. Tested float for flowthrough- ok." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 68m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk before changing handling equipment." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 68m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed conductor bails and elevator. Installed DP bails and elevator. Prepared casing tongs." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Picked up 30' conductor housing. Made up conductor housing to conductor, applied 33000 ft lbs m/u torque. Ran in with conductor to 90 m MD. Installed C-plate in rotary and landed conductor housing in same. Removed handling CART. Filled conductor with 12 m3 seawater." "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Installed C-plate on top of conductor housing. Ran 7 ea 4 3/4' aluminium innerstring joints inside conductor. Installed centralizer on joint #2. Cleared riggfloor. Picked up running CART and made up innerstring x-over. Made up CART to innerstring. Made up CART to conductor housing with 5 lefthand turns according to Vetco instruction. Installed iInclinometer and valve handle on CART. Readings on inclinometer : pitch 0,2-0,3 / roll 0,10-0,25" "On 2007-11-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed masterbushing. RIH with 30' conductor on dedicated landing string to 108 m MD. Attached sling to DP before lowering housing through Centralizer deck. Pulled condutor to oposite side of fillup valve/inclinometer and lowered conductor through deck in one continuous stroke." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 132m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Ran in with 30' conductor on dedicated landing string to 132 m MD. Filled conductor with 20 m2 seawater until returns thorugh shoe observed. Hookload after filling 109 MT." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 148m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Stung 30' conductor into funnel on F-9 while observing with ROV." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran in with 30' conductor from 148 m to 221 m MD, only minor drag in hole. Observed 112,88 m mark on landing string flush with machined ring on Centralizer deck. Meanwhile deployed hotstab line on tugger wire." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up and made up cement stand. Accidentally applied torque on TDS and put 2,5 turns righthand rotations on string. Inspected CART with ROV and backed CART in again using lefthand turns in rotary table. Performed digiquartz measurement on F-7 and F-9 indicating F-9 12 cm too high." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up cement hose to side entry sub. Adjusted height on F-9 conductor 10 cm down. Repeated elevation check on conductor housing by doing consecutive measurement on F-9 and F-7. Measured F-9 elevation 3 mm higher that F-7 - ok. Bad visiblity for establishing hotstab on template." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Poor visiblity on template base for establishing hotstab. Meanwhile tested cement line against lo-torque on side entry sub to 200 bar 10 min - ok. Made readings on inclinometer : pitch 1,3 deg / roll 0,3 deg." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- wait' and lasted for 1.0 hours. Operational details: Waited for visiblity to improve for engaging hotstab." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Removed dummy stab and installed hotstab in bank #4 on template base. Shifted lever to 'on'. Energized centralizing pistons with 2000 psi and observed travel on pistons with ROV. Made readings on inclinometer : pitch 1,27 deg / roll 0,3 deg." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Broke circulation and verified conductor full of water by observing return through fillup valve. Closed fillup valve with ROV. Hookload before circulating 87 MT." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Stepped pumps up to 1500 lpm and circulated 50 m3 seawater. Poor visiblity, assumed to be caused by returns from hole. Meanwhile performed prejob meeting prior to cementing. Hookload after circulating 97 MT." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Performed cement job. Mixed and pumped 54 m3 1,52 sg tuned light cement slurry from cement unit. Pump rate 650-750 lpm. Pump pressure 22 bar. Displaced cement with 6,5 m3 seawater to put theoretical TOC at 217 m MD inside conductor. Bad visiblity due to no current, hard to judge amount of returns from hole. Hookload after cementing 97 MT." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Rigged down cement line and flushed through manifold." "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 9.8 hours. Operational details: Waited for cement to set up. Meanwhile : -Serviced TDS -Serviced fwd and aft PRS -Changed annular element -Housekeeping, cleaning and maintenance on drillfloor" "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Waited on cement to set up. Meanwhile : -Made x-y measurements on conductor relative to funnel 36 cm/36 cm -Shifted bank #4 handle to 'off' and disengaged centralizer cylinders with 2000 psi through minireel -Retrieved hotstab and guidewire -Removed lo-torque on cement stand -Performed toolbox talk prior to releasing CART" "On 2007-11-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Slacked off 11 MT to obtain neutral at CART. Released CART by 5 righthand rotations. Lifted out CART from conductor housing and set slips on landing string." "On 2007-12-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out and racked back cement stand. Pumped 2 ea sponge balls at 2200 lpm to clean string." "On 2007-12-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Broke out an set back running CART. Pulled 4 3/4' aluminium inner string using tugger, C-plate and clamps. Meanwhile made digiquartz measurement of conductor housing elevation with ROV. F-9 24 mm lower than F-7." "On 2007-12-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed hatches in wellhead module and removed barriers. Installed hatch in moonpool. Prepared for skidding to F-1. Meanwhile installed dummy stab in bank#4 with ROV. ****Operations transferred to 15/9-F-1****" "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.0 hours. Operational details: Removed hatch on F-9 and installed hatch on F-14 in wellhead module. Meanwhile carried out pre-skidding checklist. Held toolbox talk prior to skidding rig from F-14 to F-9. Skidded rig 1.5 m port." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Cleared drilling areas and checked FWD PRS. Checked that all decks were in alignment. Rearranged hatches on F-14 and F-9." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Sent down and installed cover on funnel and moved funnel to F-9. Meanwhile picked up bit assembly and inspected same. Serviced TDS. Discovered that part of scaffolding below centralizer deck on WH module have to be removed for 17 1/2' BHA to pass on F-9." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 4.0 hours. Operational details: Waited on daylight for close standby to be able to remove scaffolding below centralizer deck in WH module. Meanwhile performed torque test on TDS and serviced equipment on drillfloor." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Removed scaffolding from below centralizer deck in WH module." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: PU and MU 17 1/2' bit, motor, 17 1/4' stab and GWD. RIH with 17 1/2' BHA to 23 m." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Continued to remove scaffolding below centralizer deck in WH module." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: MU and RIH with 17 1/2' BHA from 23 m to 156 m. Sat UHBO sleeve to high side scribe line. Stabbed into CTS on top of conductor housing while observing with ROV." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Held tool box talk with new crew. Inspected PRS dies and tested mud pump #1 using controls from drillers remote panel." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued RIH from 156 m to 196 m. Washed down from 196 m with 2000 lpm / 51 bar / 20 RPM. Tagged cement at 217.8 m. Connected CTS hose to ROV and started pumping with dredge pump." "On 2007-12-12, at Well NO 15/9-F-9, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled out 30' shoe and rathole from 217 m to 226 m MD. Drilling parameters : Flow 3500 lpm / SPP 122 bar / Rotation 40 rpm / Torque 1-3 kNm / WOB 0-1 MT. Reamed back inside shoe for every 2 m drilled. Pumped 10 m3 his-vis sweep as required to clean the hole." "On 2007-12-13, at Well NO 15/9-F-9, a drilling event occurred at a depth of 227m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 1 m new formation from 226 m to 227 m MD. Reamed hole and shoe track 3 times. No obstruction. Pulled through shoe track with no rotation. No obstruction. Pumped 10 m3 hi-vis and circulated BU while reciprocating 17 1/2' BHA." "On 2007-12-13, at Well NO 15/9-F-9, a drilling event occurred at a depth of 229m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 17 1/2' hole from 227 m to 229 m MD. Drilling parameters : Flow 4500 lpm / SPP 184 bar / Rotation 80 rpm / Torque 1-3 kNm / WOB 0-1 MT." "On 2007-12-13, at Well NO 15/9-F-9, a drilling event occurred at a depth of 229m. The activity was categorized as 'interruption -- other' and lasted for 4.8 hours. Operational details: Had oil leak in TDS. Reamed back on std and RB in derrick to have 17 1/2' bit inside shoe at 195 m. Investigated oil leak and found leaking o-ring in alignement cylinder. Changed o-ring and reinstalled cylinder. Meanwhile cleaned up oil spill on drill floor." "On 2007-12-13, at Well NO 15/9-F-9, a drilling event occurred at a depth of 195m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Changed o-ring and reinstalled alignement cylinder in top drive. Meanwhile cleaned up oil spill on drill floor." "On 2007-12-13, at Well NO 15/9-F-9, a drilling event occurred at a depth of 515m. The activity was categorized as 'drilling -- drill' and lasted for 10.5 hours. Operational details: Drilled 17 1/2' section from 229 m to 515 m MD. Drilling parameters : Flow 4400 lpm / SPP 191-195 bar / WOB 2-8 MT / Torque 1 - 5 kNm / String RPM 80/ Bit RPM 212. Average ROP 27,2 m/ hrs, max ROP 95 m/hr. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey." "On 2007-12-13, at Well NO 15/9-F-9, a drilling event occurred at a depth of 652m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' section from 515 m to 652 m MD. Drilling parameters : Flow 3440 lpm / SPP 98-100 bar / WOB 2-8 MT / Torque 1-5 kNm / String RPM 40 / Bit RPM 143. ROP 30-50 m/hr, average ROP 22,8 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey until 555 m. Sliding intervals: 515 - 535 m 555 - 565 m 595 - 610 m 635 - 653 m" "On 2007-12-14, at Well NO 15/9-F-9, a drilling event occurred at a depth of 784m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' section from 652 m to 784 m MD. Drilling parameters : Flow 3440 lpm / SPP 99-100 bar / WOB 2-8 MT / Torque 2-8 kNm / String RPM 40 / Bit RPM 143. ROP 30-50 m/hr, average ROP 22,0 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Sliding intervals: 676 - 696 m 716 - 736 m" "On 2007-12-14, at Well NO 15/9-F-9, a drilling event occurred at a depth of 830m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 17 1/2' section from 784 m to 830 m MD. Drilling parameters : Flow 3440 lpm / SPP 101 bar / WOB 5-6 MT / Torque 2-8 kNm / String RPM 40 / Bit RPM 143. ROP 20-30 m/hr, average ROP 23,0 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Sliding interval: 815 - 830 m" "On 2007-12-14, at Well NO 15/9-F-9, a drilling event occurred at a depth of 919m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 17 1/2' section from 830 m to 919 m MD. Drilling parameters : Flow 4000 lpm / SPP 124 bar / WOB 6-7 MT / Torque 5-7 kNm / String RPM 80 / Bit RPM 200. ROP 40-50 m/hr, average ROP 23,7 m/ hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Up weight 125 MT / down weight 116 MT." "On 2007-12-14, at Well NO 15/9-F-9, a drilling event occurred at a depth of 919m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pumped 30 m3 hi-vis pill followed by 30 m3 SW and another 30 m3 hi-vis pill. Pulled up to 881 m while displacing pills out with SW. Circulation parameters : Flow 3500 lpm / SPP 119 bar / Torque 3-5 kNm / RPM 80. Took survey at TD." "On 2007-12-14, at Well NO 15/9-F-9, a drilling event occurred at a depth of 919m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH to TD and displaced well to 1.40 sg bentonite mud. Staged up pump rate to 4000 lpm / 124 bar / 20 rpm / 1-3 kNm. Observed ECD level out at 1.28 sg at 5150 stks (113 m3)." "On 2007-12-14, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 9.2 hours. Operational details: Took roadmap measurement, 200 lpm / 40 rpm / 1-3 kNm. Up weight 128 MT / down weight 118 MT. POOH with 17 1/2' drilling BHA from 919 m MD to OOH. Worked through tight spots. Flushed through string with SW at 122 m with 2000 lpm. RB 17 1/2' BHA and LD 17 1/2' bit and motor assembly. Tight spots: 660 m: 15 MT overpull 371 m: 15 MT overpull" "On 2007-12-14, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PU two joints HWDP, one pup joint and cmt head. MU and RB cmt stand." "On 2007-12-15, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continued MU and RB cmt stand." "On 2007-12-15, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: Held tool box meeting prior to RU csg equipment. RU casing running equipment, 20 ft bails, elevators, csg tong, slips and FAC tool. Tested csg tong and checked torque/turn." "On 2007-12-15, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.5 hours. Operational details: Troubleshot torque/turn fault on Mærsk casing tong. No sucess. RD Mærsk csg tong and RU Odfjell csg tong." "On 2007-12-15, at Well NO 15/9-F-9, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: PU and MU shoe joint, intermediate joint and float collar joint. Thread locked connections. Checked floats in shoe and float collar for flow through with SW." "On 2007-12-15, at Well NO 15/9-F-9, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 13 3/8' csg from 36 m to 106 m MD. Filled every joint with SW. Average running speed 4 jnts/hr." "On 2007-12-15, at Well NO 15/9-F-9, a drilling event occurred at a depth of 106m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Sorted out PRS alignement problem." "On 2007-12-15, at Well NO 15/9-F-9, a drilling event occurred at a depth of 405m. The activity was categorized as 'drilling -- casing' and lasted for 7.8 hours. Operational details: RIH with 13 3/8' csg from 106 m to 405 m MD. Filled every joint with SW. Average running speed 5 jnts/hr. No tight spots encountered. Laid out 2 joints. Stabbed csg into conductor assisted by ROV. Used chain tongs in well head area to limit csg string movement and ROV used C-tool for guiding." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 754m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 13 3/8' csg from 405 m to 754 m MD. Filled every joint with SW. Average running speed 6 jnts/hr. No tight spots encountered. Up weight 127 MT / down weight 108 MT. Changed worn dies on FJE on PRS." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RD 13 3/8' csg handling equipment and RU 5 1/2' handling equipment." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 758m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: PU 18 3/4' WH housing/CART assembly and MU to 13 3/8' casing. RIH with 18 3/4' WH housing/CART assembly from 754 m to 758 m." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 758m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RD Odfjell casing tong and removed PS30 slips. Installed outer ring and master bushings." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 909m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 18 3/4' WH housing/CART assembly from 758 m to 909 m." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 909m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Attempted to land 18 3/4' WH housing into 30' conductor without sucess. Observed WH housing shoulder landing out on top of conductor." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 795m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH with 18 3/4' WH housing/CART assembly from 909 m to 795 m. Grinded off WH housing shoulder to enable stinging into 30' conductor." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 910m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 18 3/4' WH housing/CART assembly from 795 m to 909,8 m. Landed 18 3/4' WH into 30' conductor by setting down casing string weight + 5 MT to engage lock ring. Performed 25 MT overpull test. Slacked off and kept landing string in tension by an overpull of 3 MT." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 910m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Established circulation in steps with SW to 2300 lpm / 20 bar with returns on F-9 only. Kept landing string in tension by an overpull of 3 MT. Meanwhile held pre-job meeting prior to cement job." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 910m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to pump from cement unit. Pressurized TDS to 20 bar and tested line up. Released 1 3/4' preloaded ball for bottom wiper plug." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 910m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Mixed and pumped 40 m3 1.52 sg lead 1 slurry at 1200 lpm / 28 bar followed by 61,8 m3 1.52 sg lead 2 slurry at 1200 lpm / 28 bar and 15 m3 1.92 sg tail slurry at 900 lpm / 28 bar. Observed with ROV returns up F-9 only." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 910m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released top dart. Displaced and sheared sub sea wiper plug by pumping 3 m3 SW with cement unit at 1200 lpm / 10 bar. Top plug sheared after 900 ltrs / 150 bar. Zeroed counters for mud pumps and lined up to displace cement with SW using mud pumps. Displaced cement with SW at 3000 lpm. Slowed down to 1200 lpm after 2250 stks. FCP was 40 bar. Bumped plug after 2505 strokes with 128 bar. Pump eff. 96.7%. Held pressure at 128 bar / 10 minutes to test casing. Observed with ROV returns up F-9 only." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 910m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Bled of pressure and checked for backflow to cement unit. Volume bled back was 850 ltr. Disconnected cement hose after pressure had been bled off." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Reduced overpull on landing string to neutral. Released CART by 5 right hand turns and observed wellhead with ROV. Pulled above top of wellhead. LD cmt head and 6 m pup joint. MU TDS and flushed through landing string with sponge balls. Flushed sub sea template as per ROV instructions." "On 2007-12-16, at Well NO 15/9-F-9, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: LO 2 x HWDP and RB landing string in derrick." "On 2007-12-17, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued RB landing string in derrick and LO 18 3/4' CART. Cleared and cleaned rig floor area. Prepared for skidding rig to F-5." "On 2008-08-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.0 hours. Operational details: Prepared to skid rig. Skidded rig 2.25 m fwd and 1.5 m starboard to F-9. Meanwhile MU riser RT to DP std and RB same." "On 2008-08-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Lifted riser spider in to rig floor. Changed 5 1/2' handling equipment to long slings. Transported riser spider close to rotary, removed the master bushing and adapter ring. Installed the spider and hooked up hydraulic hoses and function tested same. Changed back to 5 1/2' handling equipment." "On 2008-08-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up 1st joint - TBC and stress joint, with simultaneous lift by deck crane and TDS. Checked guidewire clamp. Landed TBC and stress joint in the spider." "On 2008-08-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Picked up 1st double - lower pup joint and std joint #1 with simultaneous lift by deck crane and TDS. Removed handling flange on 1st joint. Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings. Attached guidewire slings and on TBC / stress joint." "On 2008-08-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: RIH with production riser to 20 m. Function trested TBC and performed pre-operational checks according to Vetco procedure." "On 2008-08-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Shut in F-4 and F-5 at 23:00. PU riser and TBC to rig floor and secured riser. Prepared for and opened hatch covers on all levels for F-8, F-9 and F-10." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Continued to open hatch covers on all levels for F-8, F-9 and F-10." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered boat collision stool down to centralizer deck. Prepared and lowered flow line hose down to XMT deck." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: RIH with production riser to put guidewire clamp in convenient working height at Centralizer deck. Caught guidewires and attached to ROV hooks/slings on guidewire clamp. Ran guidewires individually to 2 m above riser guide funnel at seabed. RIH to 37 m and hung off production riser in riser spider." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Picked up 2nd double - 2 ea standard joints with simultaneous lift by deck crane and TDS. Removed handling tool type E from 1st double. Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings. Meanwhile installed guide wires on template fix between F-9 and F-10 and between F-3 and F-4 using ROV. Sea current is in direction of F-13." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH with production riser to 66 m. Hung off production riser in riser spider. Removed handling flange type E." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 95m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Picked up 3rd double - lower std joint and splash zone jnt with simultaneous lift by deck crane and TDS. Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings. RIH with production riser to 95 m. Hung off production riser in riser spider. Removed handling flange type E." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up 4th double - upper pup joint and tensioner joint with simultaneous lift by deck crane and TDS. Made up connection using bolt tensioner tools. Tested flange to 3000 psi through test port - ok. Installed bolt caps and fairings. RIH with production riser to 118 m. Hung off production riser with hang off plate in riser spider. Removed handling flange. Picked up stand with premade running flange. Made up flange to tensioner joint. Picked up weight and removed hang off plate." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH on 5 1/2' DP stand to land TBC on wellhead. Observed with ROV in riser guide funnel window while coming down. Ran TBC to 10 cm above bottom of window." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Released 6 MT guidewire from template and ROV hook on riser guidewire clamp. Retrieved guidewire to surface. Released 10 MT guidewire. Hooked 10 MT guidewire on funnel. Removed RLGF." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Confirmed orientation of TBC ROV panels. Ran and established hotstab in TBC receptacle. Landed TBC/production riser on wellhead and set down 15 MT. Verified TBC fullly landed by oserving marker/band on TBC. Locked TBC connector by pressurising port A1 to 2500-3000 psi. Observed upwards movement on TBC upper body when locking TBC. Took 10 MT overpull on TBC to verify locked. Informed production to start up F-4 and F-5. Moved hotstab to port B1 and flushed lower dog cavity and upper piston cavity according to Vetco procedure." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Lined up cmt unit to standpipe to fill riser with SW while venting air through valve on top of tension joint. Closed valve. Performed pressure test of PR to 20/70 bar for 5/10 min using SW. Dropped 0.3 bar/10 min (0.4%). 447 ltrs pumped and 400 ltrs bled back. Maintained 10 MT overpull on PR throughout the operation." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Drained DP via needle valve on tensioner joint. Flushed TBC with corrosion inhibitor and retrieved hot stab to surface. Retrieved guidewires to surface and removed guidewire clamp from PR." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Lifted Norse cutting equipment down to tensioner deck and prepared line-up for installing hatches. Meanwhile prepared equipment for installing tensioner system on centralizer deck." "On 2008-08-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Re-installed hatches on F-8 and F-10." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Measured and marked groves on tensioner joint. Installed centralizer and boat collision stool in Centralizer deck. Made up contact ring. Made up tensioner assembly half hubs. Raised tensioner assembly to contact ring using tensioner cylinders." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: Continued raising tensioner assembly to contact ring using tensioner cylinders. Adjusted pressure to 90 bar and transferred tension from block to tension cylinders. Installed centralizer in Tensioner deck." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Measured and marked tensioner joint 136,0 cm above Tensioner deck. Rigged up, adjusted and dressed Norse cutting equipment on tensioner joint. Barriered off area. Adjusted block weight to put slight overpull at cut height. Drained riser through port on running flange." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Cut riser according to Norse cutting procedure. Retrieved cut part of tensioner joint. Removed riser spider. Installed outer ring and masterbushing. Broke out landing stand. Laid out cut part of tensioner joint. Installed hole cover in rotary. Meanwhile put debris barrier inside tensioner joint. Re-configured cutting jig for making bevel. Cut bevel. Used handtools to dress cut and bevel. Removed cutting jig, cleared and tidied Tensioner deck." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Installed hatch cover on F-9. BO and LO riser running tool. RU to lay out riser spider and moved to main deck. Took TDS measurements for 'riser project'." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed 4 slings in pad-eys on surface riser for dual lift in order to avoid F-4/F-5 shut-in. Lifted surface riser into drillfloor with crane and drillfloor tugger. Hooked slings on to TDS bails and picked up surface riser with top drive. Meanwhile removed hatches on F-9 and lifted Norse cutting equipment from tension deck to moonpool." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lifted multibowl onto rotary using PRS. Installed bowl protector in multibowl and lowered surface riser to connect onto multibowl. RU 2 slings from surface riser to pad-eys on multibowl for dual lift." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled master bushings and outer ring. Lowered multibowl from drillfloor to well head. Slipped multibowl over tension joint and adjusted to correct orientation STB - against F-14." "On 2008-08-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Injected and energized plastic in upper and lower BT-seals. Tested BT seals to 70 bar / 10 min - ok. Energized multibowl slips by torquing up cap screws to 600 ft-lbs." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: PU 7 MT overpull on riser/multibowl to ensure slips was locked. Released slings from TDS." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Secured surface riser with BOP horizontal tension system in moonpool. Removed handling slings from surface riser and installed split covers. Meanwhile removed rollers and trolly on HTS." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: PU and installed diverter onto surface riser. Installed outer ring and master bushings." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Waiting on MWD to troubleshoot tools and get ready to run 12 1/4' BHA. Meanwhile function tested diverter inserts and valves." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Waiting on MWD to troubleshoot tools and get ready to run 12 1/4' BHA. Meanwhile prepared for function test of diverter. Could not operate diverter bag." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Investigated diverter operation. Pulled master bushings, installed fitting on hydraulic hose. Tested system and found another leaking fitting. Changed out fitting. Re-installed master bushings." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Function tested diverter. Ok. Removed 10' diverter inserts and RB std in derrick." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk prior to PU 12 1/4' BHA. Installed link adaptor on elevators. Prepared rig floor equipment and moved 5 HWDP in derrick." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 8m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: PU and MU 12 1/4' BHA. RIH from surface to 8 m. Spinner on aft iron roughneck would not move." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 8m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Repaired aft iron rough neck spinner carriage." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 17m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: PU and MU 12 1/4' BHA. RIH from 8 m to 17 m. Not able to MU collar to powerpulse tool." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- rig up/down' and lasted for 0.5 hours. Operational details: Had to break out proper XO from back-up assembly to be able to cross over from powerpulse tool to drill collar." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: MU and RIH with 12 1/4' BHA from 20 m to 29 m." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 29m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Waiting on helicopter/crane. Meanwhile installed 10' diverter inserts." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: MU and RIH with 12 1/4' BHA from 29 m to 135 m." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Installed PS21 slips. RU auto pipe handling system." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 862m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 135 m to 862 m. Average running speed was 9 stds/hr." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 879m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: MU TDS, established circulation and washed down from 862 m with 1250 lpm and 30 rpm. Tagged TOC at 879 m. Up weight 106 MT / down weight 98 MT." "On 2008-08-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 895m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Drilled on cement/plug/float from 879 m to 895 m MD. Drilling parameters : Flow 3100 lpm / SPP 95 bar / String RPM 65 / WOB 0-4 MT / Torque 2-14 kNm / ECD 1.05 sg. Picked off bottom every 10-15 min to clean bit. Up weight 114 MT / down weight 104 MT (with pumpes off). Meanwhile RU and arranged hoses on csg tong." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 909m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Drilled on cement from 895 m to 909,3 m MD. Drilling parameters : Flow 3100 lpm / SPP 95 bar / String RPM 65 / WOB 2-3 MT / Torque 4-12 kNm / ECD 1.05 sg. Picked off bottom every 10-15 min to clean bit. Pumped 10 m3 hi-vis before connection at 902 m. Meanwhile MU and RB 9 5/8' csg. stds." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 919m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Drilled out shoe track from 909,3 m to 919,7 m MD. Drilling parameters : Flow 3100 lpm / SPP 97 bar / String RPM 65 / WOB 0-1 MT / Torque 4-6 kNm / ECD 1.05 sg. Cleaned out rathole in 2 m steps and reamed. Meanwhile MU and RB 9 5/8' csg. stds. A total of 3 stds RB in derrick." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 921m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Cleaned out rathole from 919,7 m to 921 m MD. Drilling parameters : Flow 3100 lpm / SPP 97 bar / String RPM 65 / WOB 0-1 MT / Torque 4-6 kNm / ECD 1.05 sg. Pumped 30 m3 hi-vis pill and swept the hole clean. Pulled 12 1/4' BHA into 13 3/8' csg shoe and verified no restrictions in shoe track." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: Displaced to 1.27 sg Soludril-N WBM (sized salt system) while drilling new formation. Drilled 12 1/4' hole from 921 m to 1083 m MD. Drilling parameters : Flow 3300 lpm / SPP 125-127 bar / String RPM 140 / WOB 7-9 MT / Torque 8-12 kNm / ECD 1.32-1.35 sg. Surveys taken at 991.68 m and 1049 m. Found base Utsira at 1073 as predicted. Meanwhile MU and RB 9 5/8' csg. stds. A total of 6 stds RB in derrick." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Circulated 3 x btms up while reciprocating with bit inside shale formation from 1073 m to 1082 m. Circulating parameters : Flow 3000 lpm / SPP 127 bar / String RPM 120 / Torque 5-7 kNm. Upweight 118 MT / down weight 107 MT. After 3 x btms up torque was reduced to 3-7 kNm and ECD had dropped from 1.35 sg to 1.32 sg. Meanwhile checked out equipment for POOH." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well for 15 min. Well was static. Meanwhile held tool box meeting before POOH." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 897m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Dropped 2.75' drift and POOH wet with 12 1/4' BHA from 1082 and into 13 3/8' csg shoe at 897 m. No overpull observed. Flow checked well inside csg shoe. Well was static." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 135m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Pumped 5 m3 1.40 sg brine slug and continued to POOH from 897 m to 135 m. Average pulling speed 381 m/hr." "On 2008-08-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: Pulled master bushings and removed 10' diverter inserts and PS21. Re-installed master bushings. BO and LD 12 1/4' BHA from 135 m to 2,7 m." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: BO and LD 12 1/4' BHA from 135 m to OOH. Cleaned and cleared rig floor prior to PU clean out BHA." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Serviced top drive." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Held tool box meeting. PU and MU bullnose assembly. MU and RIH with 5 1/2' DP from surface to 221 m." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 236m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: MU magnet and csg brush assembly. MU SABS circulation sub assembly. Pulled master bushings and installed 10' diverter inserts and PS21 when assemblies was below rotary. Re-installed master bushings." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 547m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued to RIH with clean up BHA on 5 1/2' DP from 236 m to 547 m." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1071m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: RIH with clean up BHA on 5 1/2' DP from 547 m to 1071 m. Broke circulation at 880 m with 500 lpm / SPP 4 bar. Upweight 98 MT / down weight 92 MT." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1082m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: MU and RIH with 2 x 5 1/2' pup- joints, TIW and air operated ball release sub. RIH and spaced out with ball drop sub in suitable position above rotary and bull nose at 1082 m. Circulated 3 x btms up while reciprocating with bit inside shale formation from 1073 m to 1082 m. Circulating parameters : Flow 3000 lpm / SPP 127 bar / String RPM 120 / Torque 5-7 kNm. Upweight 118 MT / down weight 107 MT." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1082m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated and increased pump rate in steps to 3000 LPM. String rotation 40 RPM. Reciprocated the string while circulating between 1073 m and 1082 m inside shale formation. Circulated 1.2 x btms up. Brushed hanger setting area from 848 m to 857 m." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1082m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Attached air control hose to ball release sub. Pumped 49 m3 of 1.20 SG saturated NaCl brine at 3000 lpm/127 bar. Displaced 1,28 SG Soludril-N mud from open hole and +/-150 m into 13 3/8' casing. Reciprocated the string while circulating. Released 2 1/8' ball and pumped 400 lpm at 2 bar prior to shear the SABS sub. SABS sheared at 59 bar and pressure droppet back to 2 bar, confirming that ports were open. Increased pump rate to 3000 lpm/22 bar after opening SABS and continued to circulate 120 m3 1.20 sg brine at 40 rpm while reciprocating string. Pumped the hi-vis soap train according to Halliburton procedure while reciprocating and rotating the string. Continued displacing the soap train with 115 m3 1.20 SG NaCl brine until the well was clean. NTU readings: 452/341/198/146/112." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1082m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Observed well for 30 min, well static." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 867m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: LO ball sub. Recorded up weight 105 MT / down weight 98 MT and 20 cm strech with no pumping or rotation. Rotated with 10 rpm and recorded free rotational weight 101 MT / free rotational torque 1.5-3.5 kNm. POOH wet with clean out assembly from 1081 to 867 m." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Recorded up weight 97 MT / down weight 92 MT and 10 cm strech with no pumping or rotation. Rotated with 10 rpm and recorded free rotational weight 95 MT / free rotational torque 1-2 kNm. Pumped slug brine. POOH with clean out assembly from 867 to 300 m." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 300m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Investigated and repaired oil leak on aft roughneck." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued POOH with clean out assembly from 300 to 250 m. Pulled PS21 and 10' diverter inserts." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 221m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: LO circulation sub. LO and cleaned bristle back (no dope on brush). Cleaned 445 g of swarf off magnets and LO same." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: POOH with 5 1/2' DP from 221 m to OOH." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Performed well control drill. Focused on how to set off the deluge system on rig floor and in cantiliver." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 1.5 hours. Operational details: RU for running 9 5/8' Bakerweld screens. Moved and re-installed Odfjell csg tong." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: Held pre job meeting prior to picking up 9 5/8' sand screens." "On 2008-08-31, at Well NO 15/9-F-9, a drilling event occurred at a depth of 36m. The activity was categorized as 'completion -- sand control' and lasted for 2.0 hours. Operational details: PU and RIH with 9 5/8' 13%Cr Bakerweld 250 HD screens from surface to 36 m. Lifted screens from basket on cantilever onto HTS using soft slings. Removed screen protection on rig floor. Installed centralizer and stop collar on box end on each joint." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 168m. The activity was categorized as 'completion -- sand control' and lasted for 5.0 hours. Operational details: PU and RIH with 9 5/8' 13%Cr Bakerweld 250 HD screens from 36 to 168 m. Lifted screens from basket on cantilever onto HTS using soft slings. Removed screen protection on rig floor. Installed centralizer and stop collar on box end on each joint." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 204m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: PU and RIH with 9 5/8' blank pipe from 168 m to 204 m." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 218m. The activity was categorized as 'completion -- sand control' and lasted for 2.0 hours. Operational details: Made up Screen Hanger assembly to screen liner as per Weatherford procedure. Filled PBR with hi-vis pill. up/down 93/78 MT. Installed 5½' DP slips inserts." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 218m. The activity was categorized as 'completion -- sand control' and lasted for 0.8 hours. Operational details: Held tool box talk and rigged down casing tong and cleaned rig floor." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 365m. The activity was categorized as 'completion -- sand control' and lasted for 1.0 hours. Operational details: Continued RIH with Screens on 5½' HWDP to 365 m." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1051m. The activity was categorized as 'completion -- sand control' and lasted for 2.8 hours. Operational details: Continued RIH Screens on 5½' DP from 365m to 1051m." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: At 1064 m. up/down 123/105 MT. Rigged up ball drop sub control hose and panel." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'completion -- sand control' and lasted for 0.2 hours. Operational details: Spaced out and dropped ball. Lined up and circulated ball with 200 lpm. Attempeted to set Screen Hanger." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Ball landed. Pressured up to 107 bars and held pressure for 2 min. Bled down to 70 bars. Applied 30 MT on top of liner to verify that hanger was set (70 MT on weight indicator). Attempted to set Hanger. Pulled up to leave 15 MT on running tool (85 MT on weight indicator) to shear ball seat. Started to pressure up to 233 bars to release running tool and shear ball seat. Ball seat sheared at 190 bars (7% below theoretical value 202 bars). Bled off pressure. Took pick up. New up weight 123 MT (peak at 130 MT). Up weight indicated that running tool still engaged to the hanger. Started emergency release procedure by first torqued up the drill pipe to 10k ftlbs while holding 15 MT on running tool (85 MT on weight indicator). Drill pipe started to rotate freely at approx. 2.5 kNm. Abandoned emergency release procedure. Pulled up weight (123 MT) plus additional 2.5 m to activate packer setting dogs. Set down weight to set packer. Weight lost within 20 cm. Laid down 32 MT (68 MT on weight indicator) on top of PBR to set packer. No clear indications of shear seen." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1057m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Held tool box talk and laid out Ball drop assy, DPSV and the two DP pups." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1039m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Made up to TDS and pulled up 18 m. Displaced 13 3/8' casing to 1.03 SG. 67m³ and 2500 lpm, 48 bars." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 218m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: POOH with landing string. Having Screens and Screen Hanger still attached." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 204m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Pulled up Hanger RT/ Screen Hanger and inspected same, RT sheared, no visible marks or damage." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 204m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Held tool box talk and rigged up casing tong and picked up and laid out Screen Hanger with Hanger RT." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 204m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Picked up back-up Screen Hanger and waited for go ahead. Simultaneously cleared and cleaned rig floor." "On 2008-09-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 218m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Held tool box talk and picked up and made up Screen Hanger. Rigged down casing tong." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'interruption -- other' and lasted for 4.8 hours. Operational details: RIH with 5 std 5½' HWDP and 5½' DP from 218m to 1050m" "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1059m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Picked up and made up 6 and 3 m pups." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Held tool box talk and picked up and made up drop ball sub assy." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Took up/down weight 125/107 MT. at 1064m." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Dropped ball and chased same at 200 lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Continued chasing ball, landed after 100 stks, pressured up to 107 bars and held pressure for 2 mins. Bled down to 70 bars and applied 40 MT WOB on top of liner to verify that the hanger was set (73 MT on weight indicator) and marked pipe. Left 40 MT on running tool and pressured to 178 bars to release R/T, held for 3 mins and then bled off. P/U to 125 MT. No indication of R/T was released." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1064m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Went back to setting depth and put hanger in tension 125 MT. Pressured up to 107 bars, set liner hanger and held for 3mins. Bled off pressure to 10 bars. Slacked off to 40 MT, WOB 70 MT on weight indicator to verify hanger was set, and held for 5mins. Increased pressure to 190 bars at a quicker rate and held for 3 mins. P/U to new up weight 107 MT, good indication of releasing the R/T. Slacked off to 15 MT WOB and pressured up to blow ball seat. Pressure dropped off @ 221 bars, theoretical pressure 217 bars. P/U to new up weight 107 MT and measured up 2.5 m. Slacked of 30 MT WOB. Set packer and observed 1st shear at 18 MT WOB and 2nd shear at 25 MT WOB, held for 5 mins." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 14m. The activity was categorized as 'completion -- sand control' and lasted for 2.2 hours. Operational details: Held tool box talk and laid out drop ball sub assembly, pups, TIW. Greased PS21 slips and commenced POOH from 845 to last stand HWDP." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 14m. The activity was categorized as 'completion -- sand control' and lasted for 0.5 hours. Operational details: Removed PS21 slips, 10' diverter inserts and installed master bushings." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- sand control' and lasted for 0.8 hours. Operational details: Continued POOH, inspect and laid out RT, cleared and cleaned rig floor." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 146m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Picked up swab assemblies and RIH to 146m." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 146m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Held tool box talk and pulled master bushings and installed 10' diverter inserts and ps-21 slips." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1044m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Continued RIH from 146m @ 2 mins STD, up weight 97 MT, down weight 91 MT, @ 845m continue to RIH to 1044m, picked up pup joint." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Made up to TDS, RIH to 1050, pumped 16m³ of Citric Acid, 1.06 SG @ 1500 lpm, pressure 13.7bars, displaced with 12m³ 1.03 SG brine @ 1500 lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Closed STD pipe valve, monitored well on trip tank for losses. Loss rate 260lpm dropped to 118lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 2 times with 20 m strokes 30 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 50 lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 2 times with 20 m strokes 30 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 50 lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 3 times with 20 m strokes 40 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 50 lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well 4 times with 20 m strokes 50 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 50 lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well for 10mins, 11times with 20 m strokes 50 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 250lpm." "On 2008-09-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well for 10mins, 11times with 20 m strokes 50 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 700lpm dropped to 520lpm." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Loss rate 320lpm. Filled trip tanks." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well for 10mins, 8 times with 20 m strokes 50 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Losses rate 220lpm." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well for 10mins, 11times with 20 m strokes 50 m/min. Change in drag as swabbing. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 110 lpm." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled the upper cup into the blank pipe and swabbed the well for 10mins, 11times with 20 m strokes 50 m/min. Ran back to 1050 m. Opened the stand pipe valve. Pumped 0.5 m³ down DP and displaced clean acid into well bore. Closed stand pipe valve. Let Citric acid soak. Loss rate 80 lpm." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 1050m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Lined up on 1.03 sg brine and attempted to pump down into formation. Had full return 400lpm. Total pumped 2.3m³." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 890m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Held tool box talk, lined up and POOH to 890m. Located lower swab cup inside the blank pipe." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 860m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pumped 20 m³ 1.03 SG NaCl packer fluid at 440 - 450 lpm 1.4 bar." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 840m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: POOH from 890m to 840m. Made up TDS" "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 840m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Established loss rate and monitored trip tank. Filled trip tank with packer fluid. Average loss rate 540 lpm." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 172m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Broke TDS, POOH from 840m to 172m. Filled with packer fluid via trip tank 90 m³. Pulled slowly due to U-tubing." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 172m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Held tool box talk and removed PS 21 slips and 10 inch. diverter inserts." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Continued POOH Swab assy from 172m to surface. Measured Swabs: upper 8.4' lower 8.7'." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pull bowl protector." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up bowl protector pull tool." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pulled master bushing and diverter inserts. Pulled bowl protector and laid out same." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Made up jet assy and jet well head 12-21 mtrs. 1500 lpm. 5 RPM. Pulled out and laid out jet assy." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box talk, picked up hanger assy and ran same. Verified position of orientation slot on TBG head. Pulled back to surface. 'O' ring on TBG hanger missing." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Investigated and discoustednted further action with onshore orginsation." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Held tool box talk and retrived diverter." "On 2008-09-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Hold tool box talk and rigged up to pull riser. Removed horizontal tensioning system. Attempted to pull riser." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.2 hours. Operational details: Unable to release riser from well head. Trouble shoot problem. Worked snap ring several times. Found the 12 threaded holes of the riser connector to be damaged, re-cutted the threaded holes. Made up the 12 bolt to correct distance to be able to collapse snap ring probably." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Pulled surface riser from well head. No sign of 'O' ring. Re-installed surface riser and horizontal tensioning system." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Rigged down riser handling gear. Nippled up diverter." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Installed diverter and master bushing." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Cleared and cleaned rig floor prior to ESP operation." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Held tool box talk, rigged up csg equipment and m/u swegde." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 3.5 hours. Operational details: Held tool box talk, picked up and made up ESP assembly." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Changed inserts to 7 5/8'. Picked up and made up xo jnt." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Installed control line sheave in hang off wire." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Connected control lines to motor. Pumped oil into the motor by a hand pump. Serviced the motor and evacuated the air. Connected up the electrical cable to the motor and tested out same. Made up ¼' hydraulic line from Multisensor gauge." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 16m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Leak tested ¼' hydraulic line from the Multisensor gauge to discharge pressure assembly 207 bar (3000 psi) for 10 minutes." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 16m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Cleared rig floor of redundant equipment." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 56m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Hold tool box talk. Made up 1st 7 5/8' stand of tubing from derrick to ESP assembly. Installed and function tested auto slips. Parallel activity. Retrieved riser guide funnel." "On 2008-09-04, at Well NO 15/9-F-9, a drilling event occurred at a depth of 163m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: RIH with ESP on 7 5/8' casing in stands from surface to 163m. Installed cable clamps every joint. Checked the Phoenix connection frequently. Running speed: 72 m/hr." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 699m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: Continued RIH with ESP on 7 5/8' casing in stand from 163m to 699m. Installed cable clamps every joint. Checked the Phoenix connection frequently. Running speed: 90 m/hr. Parallel activity: Injected slop in well F14." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- completion string' and lasted for 3.5 hours. Operational details: Held tool box and continued RIH with ESP on 7 5/8' casing, picked up singles from cantilever from 699m to 807m. Installed cable clamps every joint. Checked the Phoenix connection frequently. Parallel activity: Injected slop in well F14. Derrick insp. Daily maintenance Worked on flow line hose on wellhead. Performed BOP test to 15 k." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Changed elevator inserts to 5½'" "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up and make up Tubing Hanger." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Picked up complete Tubing Hanger/swivel sub assembly and made up to 7 5/8' tubing. Attempted to brake FAST connection. Modified dies to brake FAST connection." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed big wheels to casing tong due to high stick up of FAST connection." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Broke FAST connection, Orientated hanger by rotating hanger assy in FAST connector according to Schlumberger procedure, and made up FAST connection." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk, removed slips, Master Bushing and disconnected casing tong." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Installed penetrator and performed cable test to 1100 psi (76 bars) 10 min." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Spaced out and measured for cutting length of control cable." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Checked electrical down hole system before cutting main cable. Cut main cable. Spliced cable to pigtail. Checked electrical system. Parallel activity: Installed RLGF on F-15" "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk and checked equipment." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Attached penetrator to tubing hanger. Parallel activity: Continuing BOP test to 15k. Installed 4 tension cylinders F-15," "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 812m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Leak tested penetrator 'O'-rings in tubing hanger, to 69 bars for 10 minutes. Checked electrical system." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 834m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed Master bushing. RIH with Tubing Hanger and landed off at surface well head. 20.9m." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Checked electrical system. Cable resistance 2000 mega OHM. Released test lead. Installed master bushing. Backed off landing string, pulled out and laid down landing string." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed casing tong. Rigged down tubing handling equipment. Laid out running tool." "On 2008-09-05, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to rig down ESP electrical cable and sheave from derrick." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Rigged down ESP electrical cable and sheave from derrick." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk, removed redundant equipment from rig floor." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Rigged up to nipple down diverter and surface riser. Bled off diverter insert and overshot pressure." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled diverter, parked and secured same at set back area." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Rigged up to pull surface riser." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed horizontal tensioning system. Released the surface riser and pull out surface riser." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk and laid out surface riser." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared for run Tubing Bonnet/spacer spool." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to installation of Tubing bonnet/spacer spool." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up Tubing Bonnet/spacer spool and made up to dual lifting assy." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared Well head for landing off Tubing Bonnet/spacer spool. Vetco/Schlumberger" "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered down Tubing Bonnet/spacer spool. Installed same." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Leak tested Tubing Bonnet cavity to 69 bar 10 min." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Pressure tested penetrator to 69 bar 10 min." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Retrieved dual lifting assy slings from Tubing Bonnet/spacer spool. Installed Master bushing." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Signal tested Schlumberger connection. Laid out dual lifting assy slings." "On 2008-09-06, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Lowered down flowline spool piece for F9. Installed hatches in moon pool. Installed BX elevator on TDS bails. P/U spider to rig floor. Pre-check prior to skidding of cantilever from F-9 to F-15.............Handed well over to Maersk Production........." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Well handed over from production." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.0 hours. Operational details: Performed pre job meeting with involved personnel. Prepared for and disconnected surface cable." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Disconnected flow line and secured same on XMT deck." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Prepared for lifting of spacer spool." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to continue work on wellhead, crewchange." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Installed blank cap on flowline hose. Opened annulus inlet, tested port and ball valve and verified no pressure or hydrocarbons." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed TBT prior to dual lift operation of spacer spool." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.8 hours. Operational details: Disconnected and lifted spacer spool and tubing bonnet with ball valve to drill floor. Used double lift slings for the lifting operation." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Installed masterbushing. Cleaned the pulled assembly, moved same to moonpool and laid down for inspection. Meanwhile inspected wellhead prior to picking up riser." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk with all involved personnel." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Picked up riser. Removed master bushing and outer ring. Lowered riser and made up to wellhead." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Secured riser with BOP horizontal tension system in moonpool." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Held toolbox talk. Rigged up to install diverter." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Ran diverter and landed off on riser. Installed master bushings." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.8 hours. Operational details: Held toolbox talk. Rigged up sheaves in derrick for ESP cables. Rigged down diverter handling equipment." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Rigged up 5 1/2' handling equipment." "On 2009-06-24, at Well NO 15/9-F-9, a drilling event occurred at a depth of 834m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Picked up and MU hanger running tool to landing string." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 820m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: RIH to 20 m and engaged hanger. Picked up 36 ton to release hanger. Pulled up, marked landing string and racked back same." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 820m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Positioned and rigged up casing tong." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Pulled hanger through rotary. Installed master bushing. Cut cable and removed penetrator." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'workover -- completion string' and lasted for 0.5 hours. Operational details: Broke out tubing hanger and swivel sub and laid out same with running tool." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 806m. The activity was categorized as 'workover -- completion string' and lasted for 1.2 hours. Operational details: Changed to 7 5/8' handling equipment. Installed PS30 slips." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 760m. The activity was categorized as 'workover -- completion string' and lasted for 1.2 hours. Operational details: POOH to 746 m and LD 7 5/8' tubing." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 746m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Spliced rope to cable and fed same through banana sheave and back to cable spooler.Prepared DP pub and swedge." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 746m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Had TBT prior to making up DP pup and swedge to the tubing string. Made up swedge to 7-5/8' tubing string." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 746m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Attempted to break circulation, but got minimal/no flow. Continued to pressure up tubing to 67 bar. Observed no pressure drop indicating plugged tubing. Suspect pump to be plug with debris. Bled off pressure and rigged down swedge." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 138m. The activity was categorized as 'workover -- completion string' and lasted for 10.0 hours. Operational details: Held TBT prior to continue pulling 7-5/8' tubing. Pulled 7-5/8' tubing wet from 746 m to 138 m. Disconnected cable clamps and spooled power cable back to the spooling unit." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 138m. The activity was categorized as 'workover -- completion string' and lasted for 0.2 hours. Operational details: Held tool box talk with crew" "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- completion string' and lasted for 1.0 hours. Operational details: Pull out of hole laying 7-5/8' out tubing. Pulling wet. Recovered a total of 67 clamps - none left in the hole. The muddy solid filled tubing fluid was gradually becoming thicker and finally became solid just above the pump." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held tool box talk with crew" "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 21m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Cleared rig floor. Removed PS30 auto slipsand installed master bushing. Removed HTS power roller form rig floor." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 18m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Laid out last tubing joint. Pulled out ESP assemblies and removed clamps, power cable and instrument line to multi sensor. Disconnected power cable from motor." "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held tool box meeting with crew prior to manriding" "On 2009-06-25, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Carried out man riding to remove power cable and rig down sheave from derrick. Spooled power cable back on spooling unit." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 17m. The activity was categorized as 'workover -- other' and lasted for 2.8 hours. Operational details: Run back in with ESP assemblies. Disconnect bolt on discharge head c/w XO assy, pump, protector assy and motor." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Rig down Schlumberger handling equipment and Weatherford casing equipment" "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Clean and clear rig floor." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Picked up wear bushing c/w running tool. RIH to 20,9 m MD and installed wear bushing. Pulled out of hole and laid down WBRT." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Installed PS-21 auto slips and commenced to run in the hole with 5-1/2' open ended DP." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 854m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Ran in hole from 604 m to 854,5 m MD. At 850,1 m MD hang up on 9-5/8' PBR - sat down 5 tons and rotated, circulated and worked the string through PBR. At 854,5m took weight 5 tons and had no further progress. Racked back one stand." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 854m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Installed 2 x 3m DP pup joints and final stand. Removed PS-21 slips and outer split ring to wash rotary." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 892m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Washed string down from 854 m to 892 m MD. Max 2000 lpm, 5 rpm, 4-8 bar. Observed up to 9,6 % gas peak, while washing down. Reduced flow rate while filling sand traps and starting degasser and then staged up pumps. Circulated a total of 105 m3 SW prior to wash pill." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 892m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Circulated a 20 m3 soap pill around. Displaced with app. 160 m3 of SW. Parameters: Max. 4500 lpm/ 38 bar - 5 rpm. Returns clean at the end. Re-installed PS-21 slips." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Pull out of hole from 892 m to surface. Picked up single and re-installed on stand no.1." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Cleared and cleaned rig floor." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held tool box talk with involved personnel prior to rigging up for wireline logging." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Rigged up wireline cable sheaves and picked up logging tool string." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Conducted surface functional tests on Schlumberger logging tools." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 845m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Ran in hole with Schlumberger USIT-CBL logging string to 845 m" "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 660m. The activity was categorized as 'workover -- other' and lasted for 3.5 hours. Operational details: Correlated the tool and commenced to log from 845 m to surface. Got poor data in the production riser (low hydrostatic pressure). Forwarded data to onshore contact person for data interpretation. Rig personnel simultaneously carried out cleaning of header box, shakers pads, flow line and sand traps." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 170m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Ran in to 170 m and made a repeat run to surface of the riser section." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 845m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Ran in hole with Schlumberger USIT - CBL logging string to 845 m." "On 2009-06-26, at Well NO 15/9-F-9, a drilling event occurred at a depth of 695m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Carried out repeat logging pass from 845 m to 695 m." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.5 hours. Operational details: Continued repeat logging pass from 695 m to surface." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Laid out logging string and rigged down wireline equipment. Discussed barrier situation with onshore. Log interpretation to be found in 'DBR 14. Logging remarks'." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.0 hours. Operational details: Changed handling equipment for 5-1/2' DP and rigged up for running EZSV. Pick up and made up EZSV with running tool." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 50m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Ran in hole with EZSV plug on DP at 50 m.." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 366m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Ran in hole with EZSV plug on DP to 366 m." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 878m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.8 hours. Operational details: Toolbox talk with new shift. Ran in from 366 m to EZSV setting depth 878 m. Running speed 1,5 min/std, filling pipe every 5 stds." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 878m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Position EZSV plug at 878 m in neutral weight (=95 t). Sat EZSV and observed sleeve to shear at 117 ton. RIH and tagged the EZSV with 10 t - OK." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Pulled out of hole with running tool from 878 m to 15 m." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Changed out PS-21 slips to master bushing and laid out EZSV running tool" "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.5 hours. Operational details: Had Tool box talk prior to picking up RTTS Made up side entry sub assembly. PU and MU Halliburton RTTS assembly and confirmed same to be open." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 219m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.0 hours. Operational details: Ran in hole to 222 m. Flushed RTTS packer sealing interval with SW 400-800 lpm. Position RTTS at 219 m and set same." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 219m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Made a line test 200 bar OK. Pressure tested the RTTS to 126 bar/10 min. OK. Volume pumped/returned 349 l." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 11m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: Rigged down cement hose and released RTTS packer. Pulled out of the hole from 219 m to 11 m." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Laid out RTTS assembly. Cleared and cleaned rig floor." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held toolbox talk with crew prior to running in hole with 3-1/2' DP" "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Rigged up handling equipment for 3-1/2' DP. Grease equipment." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 319m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Made up cement stinger to string and ran in hole to 319 m." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 875m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: Change handling gear to 5-1/2' DP and ran in hole from 319 m to 875 m. Circulated btms up at 4000 lpm and 138 bar." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 875m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Held tool box talk to crew prior to cement job" "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 875m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Laid out single and installed 3m pup, side entry sub and FOSV onto string. Made string up to TDS. Confirmed line up and conducted line test 200 bar/5 min." "On 2009-06-27, at Well NO 15/9-F-9, a drilling event occurred at a depth of 875m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pumped 20 m3 DW as a spacer. 2000 lpm/42 bar with mud pump." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 875m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Mixed and pumped 16,8 m3 1,9 sg slurry 800 lpm with cement unit. Displaced cement with 5,1 m3 of DW with cement pump (1200 lpm). Cement plug set in the interval 650-878 m." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 540m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Removed cement hose and racked back cementing assembly. Flushed lines. Pulled out of hole from 875 m to 540 m. 3 min/std." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 540m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed 2 ea sponge balls in string and circulated 1,5 x string volume. 130bar/4000 lpm." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 540m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Picked up cementing assembly. Ran in hole and laid out same. Made up single to string and racked back same." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 319m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pulled out of hole from 540 m to 319 m. Change handling equipment to 3-1/2' DP." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: Pulled out of hole from 319 m to surface. Racked back cement stinger. Changed handling equuipment to 5-1/2' DP." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 7m. The activity was categorized as 'plug abandon -- wait' and lasted for 1.0 hours. Operational details: Changed handling equipment and picked up 12-1/4' mill assembly and ran in hole to 7m." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 7m. The activity was categorized as 'plug abandon -- wait' and lasted for 0.2 hours. Operational details: Tool box talk with new crew prior to running 12-1/4' mill assembly" "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 131m. The activity was categorized as 'plug abandon -- wait' and lasted for 2.8 hours. Operational details: Continued to make 12-1/4' millling BHA. - changed out master bushing to PS-21 slips" "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 480m. The activity was categorized as 'plug abandon -- wait' and lasted for 0.8 hours. Operational details: Ran in to 480 m and observed no obstructions while running in." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 131m. The activity was categorized as 'plug abandon -- wait' and lasted for 0.8 hours. Operational details: Pulled out of hole from 480 m to 131 m - broke circulation and observed clean returns." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 2.0 hours. Operational details: Changed PS-21 slips to master bushing- laid out and rack milling BHA. Note: Cement fully set up at 13:30 hrs" "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Held toolbox talk prior to handling 3-1/2' DP - rigged up for 3-1/2' DP" "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 319m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Held toolbox talk and ran in to with cement stinger on 3-1/2' DP to 319 m." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 610m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Changed handling gear from 3-1/2' to 5-1/2' and continued to run in from 319 m to 610 m" "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 655m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Washed down 2000 lpm from 610 m to 655 m.- tagged hard cement at 655 m and sat down 5 ton." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 655m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Held tool ox talk prior to setting cement plug whilst re-calculating the space out for side entry sub Spaced out DP and installed side entry sub." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 654m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Circulated 10 m3 of DW with rig pumps and verified line up from cement unit" "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 654m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Mixed and pumped 5,1 m3 of 1,90 sg 'G' cement slurry at 800 lpm. Displaced the cement with 4,6 m3 DW at 1200 lpm (cement pump). Cement plug placed in interval 655-590 m. Broke out cementing assembly." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 469m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pulled from 654 m to 469 m with 3 min/std. Pulled stds dry." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 469m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Inserted 2 ea sponge balls in string. Made up TDS and circulated 1,5 x string volume at 2500 lpm." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Pulled out of hole from 469 m to 319 m. Change handling gear from 5-1/2' DP to 3-1/2' DP. Pulled out to surface and laid cement stinger." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Cleared rig floor and changed handling equipment from 3-1/2' to 5-1/2' DP. Broke down cement stinger." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Held tool box talk to discuss handling of whipstock and test of Multifunction Bypas Valve" "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Made up Multicycle Bypass valve. Installed XO on top and btm + TIW ." "On 2009-06-28, at Well NO 15/9-F-9, a drilling event occurred at a depth of 40m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Ran in hole Multi Cycle Bypass Valve on one stand. Attempted to function test the valve." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 40m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Pumped 4,5bar/500 lpm, 4,5bar/1000 lpm, 12bar/1500 lpm, 26bar/2000 lpm. Tool failed to operate. Repeated pressure sequences a second time with no success. Made two pressure cycles with 26 bar/2000 lpm and 40bar/2500 lpm. Tool failed to operate." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 40m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Decided to change to back-up tool. Changed out primary to back-up Multi Cycle Bypass Valve." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 40m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: Pumped 4,5bar/1000 lpm, 20bar/2500 lpm. Tool failed to operate. Repeated pressure sequences a several times with no success." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 205m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Ran in hole to 205,5m with Multi Cycle Bypass Tool" "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 205m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Attempted to cycle Multi Cycle Tool with 18 bar/2500 lpm. No go. Repeated cycles with 1 min intervals between dipping pumps rather than 3 min. Observed +10 bar pressure spike every 3 rd cycle, but tool is not closing/activating." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 205m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Discussed options with town. Carried out house keeping and PM projects." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 207m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Discussed Multi Cycle By-pass Valve (MCBV) operational problems with service companies and town." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 5.5 hours. Operational details: Attempted several times to cycle MCBV. Pulled out of hole from 207 m to surface. Broke out and laid out MCBV. Simultaneously had discussion and meeting with town regarding modified procedure and BHA configuration. Decided to take out MCBV and orient Whipstock with gyro on wireline." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Tool box talk with crew prior to making up Whipstock assembly" "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 266m. The activity was categorized as 'plug abandon -- mill' and lasted for 5.5 hours. Operational details: Picked up and made up 13-3/8' TrackMaster Whipstock assembly with 12-1/4' Mill BHA. Surface to 266 m.Verified UBHO toolface offset and whipstock scribe lines." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 432m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Ran in hole with Whipstock assembly from 266 m to final setting depth 432 m. Took 2 ton weight at 274 m but dropping off." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 432m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Held tool box talk with crew prior to rigging up wireline." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 432m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Rigged up wireline sheaves and picked up Gyro tool. Ran in hole with Gyro to 402 m (UBHO sub). Found tool face orientation to be 178 deg. Rotated string to 190 deg. Confirmed by Gyro." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 432m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Pulled out with wireline and confirmed tell tale ok on Gyro. Moved string up/down twice to work out torque. Up/down weight 108/104 ton." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 432m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: Ran in hole with gyro on wireline to 402m. Found tool face to be 187 deg. (target =190 deg +/- 5 deg). Pulled out wireline and gyro." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 432m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: On final position screwed in with TDS. Pressured up the string to 253 bar/10 min to set the Whipstock slips. Observe hook load decrease from 106 t to 99 t. Proper setting confirm by setting down 10 t and applying over pull 10 ton. Pulled 140 ton (32 ton overpull) to shear bolt for 12-1/4' FastTrack mill. Confirmed mill to be free." "On 2009-06-29, at Well NO 15/9-F-9, a drilling event occurred at a depth of 416m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Laid out 2 ea 3 m pup joints and made up one stand to string Midnight depth 416 m." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 422m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Made up string to TDS. Took off bottom parameters up/down 105/102 tons. Tagged whipstock at 421,5 m. (=top of window). Commenced drilling window. Initially exprienced heavy vibration in string. Experienced an hydraulic leak on TDS." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 422m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Observed hydraulic leak on elevator. Pulled back to 417 m and fixed leak." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 422m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Milled window in 13-3/8' casing according to instructions from Smith: Flow 1500 lpm / SPP 66 bar / String RPM 80 / WOB 1-2 MT / Torque 16-21 kNm" "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 422m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Milled window in 13-3/8' casing 422,0-422,1m: Flow 2170 lpm / SPP 92 bar / String RPM 80 / WOB 3,5 MT / Torque 8-12 kNm" "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 423m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Milled window in 13-3/8' casing 422,1-422,8 m: Flow 2170 lpm / SPP 93 bar / String RPM 90 / WOB 5,0 MT / Torque 8-15 kNm . Pumped Hi-vis sweep" "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 423m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Milled window in 13-3/8' casing 422,8 - 423,0 m: Flow 2170 lpm / SPP 88 bar / String RPM 95 / WOB 5,0 MT / Torque 12-18 kNm" "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 424m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Milled window in 13-3/8' casing 423,0 - 423,8 m: Flow 2170 lpm / SPP 88 bar / String RPM 100 / WOB 4,5 MT / Torque 11-14 kNm Circulate Hi-vis sweep and got 100% steel back (no formation)" "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 424m. The activity was categorized as 'plug abandon -- mill' and lasted for 5.0 hours. Operational details: Milled window in 13-3/8' casing from 423,8 - 424,3 m as per Smith instructions: Time Depth (m) Flow (lpm) SPP (bar) RPM WOB (MT) Torque (kNm) 07:00 423,8 1525 50,5 60 5-6 14-17 09:00 424,2 1900 73,5 105 6 13-18 10:00 424,3 1900 74,0 125 5-10 19-22 10:30 424,3 1900 72,9 125 9-11 25-31" "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 424m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Observed instant drop on 50 bar in SPP. Pulled out of hole from 424,3 to 266 m." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 266m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Due to drilling with severe vibration inspected and serviced TDS for loose items. Carried out derrick inspection." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Continued to pull out from 266 m to surface." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Found 8-1/8' XO 6-5/8' FH B x 6-5/8' REG P parted 0,17m above pin end. (SN.03154H). 7,02 m fish (WIndow mill + water melon mill) left in hole. Top of fish 417,3 m. Broke out remaining BHA." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 5.5 hours. Operational details: Spotted and prepared fishing tool (11-1/4' overshot with extension sub and 9' grapple). Welded and machined overshot lip guide. Simultaneously carried out further inspection and maintenance on TDS. DNV inspected Poorboy, degasser and tugger." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.0 hours. Operational details: Observed loose die holder and worn dies on TDS pipe handler. Repaired same." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Made up XO to 11-1/4' fishing overshot." "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Held tool box talk with crew" "On 2009-06-30, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: Continued making up fishing BHA including 11-1/4' fishing overshot with 9' grapple. Midnight depth = 0 m." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Made up fishing BHA and installed PS-21 slips and sensor on AR." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 410m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Ran in with overshot from surface to 410 m." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 417m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Made up TDS to string and took up/down weight 83/80 ton and free rotation 750 Nm. Ran in to 415 m and circulated 2000 lpm/4,4 bar over fish. Reduced flow rate to 1000 lpm and rotated 10 rpm. Moved down over fish at 417 m. Tagged fish and observed increase in pump pressure and torque.Stopped pumps and rotation. Sat down 10 ton." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: Picked up and observed additional 2 ton pick up weight. Pulled out slowly from 424 m to 20 m." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Held tool box talk with crew regarding laying out overshot with fish." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Retrieved overshot with attached fish. Transferred complete assembly including fish from vertical to horizontal. Decided to backload overshot and fish to town for disassembly. 12-1/4' FastTrack TRI mill was completely worn out." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Held Tool Box Talk with crew prior to making up milling BHA." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Commenced to make up 12-1/4' TrackMaster milling assembly." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 76m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Made up 12-1/2' TrackMaster milling BHA" "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 417m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: Ran in hole with TrackMaster mill from 76 m to 417 m." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 417m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.5 hours. Operational details: Prepared pit and surface flow system for displacment to milling mud. Flushed and cleaned pits and conditioned milling mud." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 417m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Displaced the well to milling mud with 2000 lpm / 29 bar." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 428m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.2 hours. Operational details: Took parameters: Up/down weight 106/102 ton - RW 104 ton with 2kNm. Started milling from 424 m to 428 m as per Smith instructions: Time Depth (m) Flow (lpm) SPP (bar) RPM WOB (MT) Torque (kNm) 12:00 424,3 1900 28,0 90 1 9-20 13:00 424,5 2370 39,0 110 5-6 9-14 14:00 426,3 2390 40,0 110 5-6 6-9" "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 428m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Milled out of casing at 428,2 m. Window = 421,5 m (top) and 428,2 m (btm). Reamed interval 428 m - 420 m." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 419m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: While reaming 428 m-420 m observed dropped object from derrick. Stopped rotation and pulled to 419 m. Circulated bottoms up at 3000 lpm / 59 bar. Bolt dropped down on rig floor from derrick." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 416m. The activity was categorized as 'interruption -- maintain' and lasted for 5.0 hours. Operational details: Racked back stand - depth 416 m and investigated dropped object. Meanwhile monitored well on trip tank. A 0,17 kg bolt had loosened and unscrewed from the TDS and dropped 30 m to rig floor (50 Joule). Re-installed bolt and lock wire. Changed out other damaged lock wires. Further investigated for loose items and potential dropped objects." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 428m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Ran in from 416 m to 428 m." "On 2009-07-01, at Well NO 15/9-F-9, a drilling event occurred at a depth of 435m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.8 hours. Operational details: Drilled formation and opened window with 12-1/4' string mills from 428 m to 435 m. Time Depth (m) Flow (lpm) SPP (bar) RPM WOB (MT) Torque (kNm) 22:00 430,0 2390 44,0 110 0-1 7-9 24:00 435,0 2370 46,0 110 0-1 6-9" "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 436m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.0 hours. Operational details: Continued to drill formation to 436,5 m and reamed window according to instructions from Smith Rep. Reamed window several times from 421m to 436m - 2500 lpm - 42 bar -90 rpm - 5-9 kNm. Stopped pumping and rotation and slided in from 421m. Taking weight and held up at 421 m and 425 m. Positioned water melon string mill in window and milled further in the interval 420 - 428 m. Slided through window with milling string, still picking up a few tons of weight at 421 m and 425 m, however a slight rotation (app. 90 deg) allowed the string to slide through window. In total 14,4 kg has been recovered from the ditch magnets." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 436m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: Pumped 20 m3 SW spacer and displaced milling mud to 1.20 KCL/polymer mud. Circulated 74 m3 KCL mud. Filled trip tank." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 436m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Flow checked the well. Simultaneously checked TDS for loose items." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 200m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Pulled out of hole with milling assembly from 436 m to 200m" "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 132m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Pulled out of hole with milling assembly from 200 m to 132 m." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.8 hours. Operational details: Pulled out of hole with BHA from 132 m to surface. Gauged mills: Starter mill 3/8' under gauge, follow mill 3/4' under gauge, melon mill ½' under gauge. Laid out window milling assembly." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Cleaned and tidied rig floor." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Made up 12-1/4' Trackmaster milling BHA." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: Inspected TDS for potential falling objects." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 266m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.0 hours. Operational details: Ran in hole with Trackmaster mill from 20 m to 266 m." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 414m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Ran in hole with Trackmaster mill assembly on 5 ½' DP from 266 m to 414 m." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 414m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Recorded parameters: Up weight 106 tons, down weight 103 tons, rotation weight 105 tons with 80 rpm and 2 kNm." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 435m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Washed down from 414 m to 425 m with 500 lpm, 6 bar. Took weight at 425 m. Rotated past obstruction with 10 rpm and 1-4 kNm from 425 m to 427 m. Washed down from 427 m to 433 m. Took weight at 433 m. Rotated past obstruction with 10 rpm and 1-4 kNm from 433 m to 435 m." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 435m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: Polished the interval from 420 m to 435 m with 2000 lpm, 41 bars, 80 rpm and 1-4 kNm. Polished the interval two times." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 435m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Stopped rotation and washed the interval from 420 m to 435 m with 2000 lpm, 41 bars. Washed the interval two times." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 422m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Stopped pumping and slide mill assembly through window two times. Took 4-5 ton weight at 423, 5 m when moving downwards through window. (Whipstock fishing groove). Rotated through window with 1 rpm without taking weight." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 266m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Pulled out of hole from 422 m to 266 m." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.2 hours. Operational details: Pulled out of hole with BHA from 266 m to surface. Gauged mills: Starter mill 1/8' under gauge, follow mill 1/16' under gauge, melon mill in gauge. Laid out window milling assembly." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Cleaned and tidied rig floor." "On 2009-07-02, at Well NO 15/9-F-9, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Held pre job meeting. Picked up and ran in hole with 12 ¼' BHA to 32 m." "On 2009-07-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Ran in hole with 12 ¼' BHA from 32 m to 190 m." "On 2009-07-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Installed hydraulic power slips. Found leak on hydraulic connection." "On 2009-07-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 190m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Repaired power slips." "On 2009-07-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 400m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Ran in hole with 12 ¼' BHA on 5 ½' DP from 190 m to 400 m. Filled pipe." "On 2009-07-03, at Well NO 15/9-F-9, a drilling event occurred at a depth of 430m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Ran in hole from 402 m to 430 m. No weight taken when passing through window. Established circulation and tested the MWD with 2500 lpm, 73 bar. ***End of operation for F - 09***" "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Transferred over from well F-99. Broke out 5 1/2' DP pup on 30' conductor running tool and prepared subs for cement assembly stand. Requested production to shut-in wells F-7, F-12 and F-14. Meanwhile: ROV performed template survey. Prepared to P/U 36' hole opener assembly. Mixed Hi-vis spud mud" "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: M/U cement assembly stand and attempted to rack back same. Unable to pass below derick PRS beam. Production confirmed wells F-7, F-12 and F-14 shut-in at 03:15 hrs." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Broke out lower Full Open Safety Valve on cement assembly stand and racked back same." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: M/U conductor running tool to 5 1/2' HWDP and racked back same. Meanwhile: Removed F-11 weather deck hatch cover." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held pre-job safety meeting prior to P/U 36' hole opener assembly." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: P/U 36' hole opener assembly and set same in rotary table." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Held pre-job safety meeting prior to picking up 36' BHA. Picked up and made up Gyro Track and ran in hole to 25m. Unable to lower 36' BHA through weather deck hatch due to alignment problem." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 25m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Troubleshoot alligment problem. Removed rotary master bushing to enable 36' BHA to pass through weather deck hatch." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 93m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: Picked up and made up 36' BHA and run in hole same from 25m to 93m. Notified Production that well F-14 could be reopened after 36' BHA run below centralizer deck (lowest Volve platform deck)." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 93m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held pre-job safety and DOP meeting with rig crew and all involved service personel prior to spud." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Ran in hole with 36' BHA on 5 1/2' HWDP from 93 m to 120m." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 144m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Ran in hole with 36' BHA on 5 1/2' HWDP and entered F-11 subsea template funnel. RIH and tagged seabed at 143.97 m RKB and spudded well (at 17:25 hrs.)." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 146m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: Established circulation and washed down with 600 lpm, 3 bar, 0 rpm, WOB 0 MT from 144 m to 146 m. Increased flow rate to 1000 lpm, 3 bar, WOB 1-2 MT and observed firm formation. Meanwhile: Held pre-spud meeting with all rig night shift personnel. Held DOP meeting with on comming new drill crew." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Established drilling parameters at 1500 lpm, 10 bar, 30 rpm, 2 KNm, WOB 0-1 MT and drilled from 146 m to 147 m. Picked off bottom and adjusted drilling parameters due to high vibrations." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 160m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 36' hole from 147 m to 160 m. Drilling parameters: 1500 lpm, 11 bar, 40 rpm, 5 KNm, WOB 2-3 MT, Gross ROP 6 m/hr. Pumped and cleaned hole with 10 m3 Hi-vis pill." "On 2013-03-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 36' hole from 160 m to 165 m. Drilling parameters: 3400 lpm / 76 bar, 60 rpm / 5-10 KNm, WOB 2-3 MT, Gross ROP 5 m/hr. Inclination survey: Bit depth 161 m (Ontrack sensor at 147.6 m) 0.22 degrees Bit depth 165 m (Ontrack sensor at 151.6 m) 0.16 degrees" "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 177m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 36' hole from 165 m to 177 m. Drilling parameters: 3400 lpm, 73 bar, 60 rpm, 3-8 KNm, WOB 2-3 MT, Gross ROP 4 m/hr. Inclination survey: Bit depth 174 m (Gyro sensor at 151.6 m) 0.35 degrees Bit depth 174 m (Ontrack sensor at 160.6 m) 0.07 degrees Pumped and clean hole with 17 m3 1.03 sg. Hi-vis pill." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 36' hole from 177 m to 197 m. Drilling parameters: 3400 lpm, 77 bar, 70 rpm, 4-8 KNm, WOB 2-3 MT, Gross ROP 7 m/hr. Inclination survey: Bit depth 183 m (Gyro sensor at 160.5 m) 0.09 degrees Bit depth 183 m (Ontrack sensor at 170.1 m) 0.03 degrees Bit depth 192 m (Gyro sensor at 169.3 m) 0.18 degrees Bit depth 192 m (Ontrack sensor at 178.9 m) 0.07 degrees Pumped and clean hole with 10 m3 1.03 sg. Hi-vis pill." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 36' hole from 201 m to section TD at 208 m (36' TD 203.9 m). Drilling parameters: 3300 lpm, 77 bar, 70 rpm, 4-8 KNm, WOB 2-3 MT, Gross ROP 7 m/hr." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pumped 25 m3 1.03 sg. Hi-vis pill and circulated same out of hole." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Recorded section TD survey. Inclination survey: Bit depth 207 m (Gyro sensor at 184.6 m) 0.18 degrees Bit depth 207 m (Ontrack sensor at 194.2 m) 0.10 degrees Meanwhile: ROV attempted to verify correct TD depth by observing painted mark on DP relative to top of F-11 template funnel, unable to check position of DP mark due to poor visibility." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Displaced hole with 60 m3 1.40 sg mud at 3300 lpm, 90 bar, 5 rpm." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 152m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: POOH to 4 m below sea bed to 148m. Perfomed wiper trip from 148 m to TD at 208 m, no down wt recorded while RIH and no fill found on bottom. Displaced hole with 60 m3 1.40 sg mud at 3300 lpm, 90 bar. 5 rpm. POOH to 152 m and topped up well with 5 m3 1.40 sg mud. Recorded TD Survey: Bit depth 207 m (Gyro sensor at 184.6 m) 0.18 degrees Bit depth 207 m (Ontrack sensor at 194.2 m) 0.10 degrees" "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 152m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed Derick and Top drive systems inspection." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 152m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Held pre-job meeting. Removed weather deck spilt hatches to enable passing of 36' BHA." "On 2013-03-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 152m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: WOW: Evaluated weather situation with town. Decision made to keep 36' hole opener assy at secure depth within template funnel and wait on WOW to minimise risk of damage to adjacent production risers POOH 36' BHA. WOW: Wind Sea Hz Sea max Dir(deg)/(Kts) (m) (m) 15:00 106/28 5.2 8.4 16:00 104/26 5.0 8.1 17:00 108/26 5.0 8.3 18:00 106/25 5.0 8.0 19:00 107/25 4.7 7.5 20:00 106/25 4.9 7.8 21:00 105/26 4.4 7.0 22:00 106/23 4.5 7.2 23:00 103/21 4.4 7.0 Meanwhile: Prepared to run and cement 30' conductor. Serviced drilling equipment." "On 2013-03-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 152m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: WOW with 36' hole opener assy at secure depth within template funnel: WOW: Wind Sea Hz Sea max Dir(deg)/(Kts) (m) (m) 00:00 103/21 4.4 7.0 01:00 103/21 4.0 6.5 02:00 106/20 4.1 6.5" "On 2013-03-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held pre-job meeting prior to perfoming wiper trip. RIH from 152 m, observed string jump when first starting to RIH. Later observed that string had parted." "On 2013-03-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Held pre-job meeting prior to perfoming wiper trip. RIH from 152 m to TD at 208 m, observed string jump when first starting to RIH. Observed mark on DP at rotary table indicating 36' BHA on bottom, set down 2-3 ton to tag same. Depth tag at bottom indicated no fill. Pumped 50 m3 1.40 sg mud to displace hole, 3200 lpm, 22 bar. 5 rpm. Meanwhile: monitoring weather conditions. Wind Sea Hz Sea max Dir(deg)/(Kts) (m) (m) 03:00 106/19 3.8 6.0 04:00 105/18 3.8 6.1" "On 2013-03-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 198m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Started POOH 36' BHA from TD at 208 m. ROV moved towards F-11 well centre to observe POOH and observe 36' hole opener assy had detached from string. ROV checked template and observed 36' hole opener fish sticking up out of F-11 well slot with top of fish approximately flush with top of F-11 guide funnel (Top of Fish (TOF) at ca. 140,20 mRKB)." "On 2013-03-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: Evaluated risk of POOH recoverable section of BHA up through Volve Platform. Held pre-job meeting. POOH and found that BHA had parted at a service break connection on the jar body. From recovered section of BHA estimated fish length to be 58,52 m, approximately 14 ton (in air). Evaluated situation and discussed same with town. Meanwhile: ROV pulled back to safe area 50 m from F-11 well centre while POOH BHA." "On 2013-03-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 12.5 hours. Operational details: Discussed situation with town. Mobilized fishermen and fishing equipment. ROV attempted to observe TOF in guide funnel, poor visibility in template area. Meanwhile: ROV surveyed of risers, no damage observed. Survised drilling equipment and took onboard bulk from supply vessel." "On 2013-03-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Fisherman and fishing equipment arrived at rig onboard two helicopters (arriving 22:30hrs and 22:38hrs). Prepared fishing equipment. Meanwhile: ROV perform template survey with poor visibility and found section of BHA laying on sea bed next to template." "On 2013-03-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: Evaluated situation and investigated further to determine details of fish in hole and laying on sea bed. Using a serial no. observed on top of fish at template funnel identified that the upper most part of the fish was a 9 11/16' OD wear sleeve which forms the upper part of 11 3/4' stabilizer on the OnTrack tool. Length of fish in hole re-calculated to be 11,90 m, approximately 4-5 ton (in air). Length of BHA on seabed estimated to be 46.62 m. approximately 7 ton (in air)." "On 2013-03-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 16.0 hours. Operational details: Evaluated situation and discussed same with town. Prepared plans for various fishing scenerios and mobilized additional equipment. Sent spud boat Olimpic Torres to town to collect additional fishing equipment. Additional fisherman arrived at rig onboard helicopter at 19:51 hrs. Meanwhile: Completed Enviro Unit installation. Pulled ROV back on deck, adjusted to acheive neutral bouyancy, serviced equipment and upgraded software prior to installation of Digiquartz depth sensor. Performed general rig maintanence." "On 2013-03-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: Worked on preparation of fishing operation risk assesment. Fishing equipment ETA. 10:30 hrs." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: Conducted fishing operations risk assessment. Meanwhile: Spotted wireline unit on cantilever deck. Performed general rig mainenance." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: Waited on additional fishing equipment to be delivered to rig on spud boat Olympic Taurus ETA 10:30 hrs. 11/03/13 Meanwhile: Performed general rig maintenance, build reserve spud mud and Hi-vis pill and commisioned MI-Swaco Enviro unit." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 5.5 hours. Operational details: Evaluated situation and discussed same with town. Prepared plans for various fishing scenarios and worked on risk analysis for same. Additional fishing equipment arrived at rig onboard spud boat Olympic Taurus at 11:10 hrs. Offloaded spud boat Olympic Taurus and transfered fishing equipment to cantilever deck." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: Prepared fishing BHA with rotary cover inplace. In discussion with town finalised configuration of first fishing run. Performed risk assesment of same and presented to onshore/offshore management. Requested production to shut-in wells F-7, F-12 and F-14 at 14:30 hrs. Meanwhile: Prepared for fishing operations. ROV observed fish slipping down ca. 20 cm/hr inside template guide funnel." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: Held pre-job meeting with all involved personal. M/U fishing BHA spear assembly to attempt to engage 3' ID opening at top of fish. Production confirmed wells F-7, F-12 and F-14 shut-in at 16:01 hrs." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 141m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: Removed hatches on lower decks and hole cover. RIH to 80 m with 2 13/16' ITCO Spear fishing assembly on 5 1/2' DP to 137 m. ROV located fishing assembly observed same as string was lowered down to above TOF to 141 m Called in ROV to inspect Top of Fish (TOF). Meanwhile ROV positione to guide 2 13/16' ITCO Spear into funnel guide." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: Attempted to engage 2 13/16' ITCO Spear into fish. ROV guided 2 13/16' ITCO Spear bull nose ca. 5 cm into opening TOF at 143 m (Note: Seabed at 144 m). Worked string 5 rpm, 2KNm, set down weight 0-2 MT and attempted to RIH spear grapple into TOF and engage same. Pulled back and inspected TOF and bull nose with ROV. Evaluated situation, informed production that fishing assembly would be POOH." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: POOH from 139 m to surface. L/O 2 13/16' ITCO Spear and M/U 2 1/2' - 3 5/8' Taper Tap." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Evaluated situation and prepared detailed operations procedure." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 138m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: Held pre-job meeting. Attached ROV handling sling to 2 1/2' - 3 5/8' Taper Tap assembly and secured same. Informed production of forward fishing operation and RIH to 138 m observing fishing string with ROV from 75 m to template. Recorded Up/Down weight 76/72 MT. Meanwhile: ROV visual from 75m to template at seabed." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 143m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: RIH taper tap assembly and entered TOF at 143 m. Engaged fish with 2 1/2' - 3 5/8' Taper Tap assembly with 5 rpm, 3 KNm in 2' increments into fish." "On 2013-03-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 130m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Picked up 8 MT and confirmed 2 1/2' - 3 5/8' Taper Tap assembly engaged in TOF. Pulled out with fish to above guide funnel. ROV engaged pre-made sling and pulled fish clear of template. Lowered fish and set down same on seabed. 2 1/2' - 3 5/8' Taper Tap assembly disengaged and fish layed down on seabed. - Fish located 11 m clear of template, fish heading 300 degrees orientated forward - aft under rig." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 130m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: ROV performed site survey and confirmed fish location. Fish location 11 m from template heading 300 degrees orientated forward - aft under rig.." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: POOH from 130 m to surface. B/O and L/O 2 1/2' - 3 5/8' Taper Tap assembly." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Cleaned and Cleared rig floor. Meanwhile: Removed moonpool spilt hatches and mobilized 36' BHA handling equipment to the rig floor for wiper trip." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 7m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Held pre-job meeting. P/U and M/U 36' hole opener assembly for wiper trip (Similar stiffness to 36' drilling BHA without OnTrack and Gyro Track) and centralizer drill bushing." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 153m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: M/U 36' BHA and RIH on 5 1/2' DP from 7 m to 153 m. ROV observed 36' BHA running down to template and entering F-11 template funnel." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 154m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Recorded down weight at 153.7 m, 1-2 MT. Attempted to rotated pass hang up depth, 0 lpm, 0 bar, 5 rpm, 5KNm, WOB 3 MT. NoGo" "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Picked up and established parameters. RIH, washing and rotated down from 153 m to TD at 208 m with 1000 lpm, 4 bar, 10 rpm, 1-2 KNm, WOB 1-2 MT tagged bottom at 208 m with 3 MT. No restriction or fill encountered from 155 m down to TD." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pumped 25 m3 1.03 sg Hi-vis pill, 1600 lpm, 15 bar, 10 rpm, 1-2 KNm . Recipricated string and circulated 1.03 sg Hi-vis pill out of hole, SW, 3380 lpm, 60 bar." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Displaced well to 1.40 sg mud, 3300 lpm, 70 bar, 19 rpm, 1-2 KNm while reciprocating string and POOH from TD at 208 m to 145 m just below seabed. - No restrictions observed while POOH from TD." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Performed wiper trip. RIH 36' assembly from 145 m to TD at 208 m. Displaced well to 1.40 sg mud with 3360 lpm, 70 bar, 10 rpm, 1-2 KNm while rediprocating string. Continued to POOH to 145 m and top up hole with 1.40 sg mud. Meanwhile spotted casing equipment on cantilever deck. Held Detailed Operations Plan (DOP) meeting with offshore and onshore personel for running 30' conductor." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Held pre-jog meeting. POOH from 145 m to 16 m with 36' BHA and racked back DC stands. Pulled master bushing and pulled out centralizer drill bushing 36' hole opener assembly and layed out same." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held pre-job meeting for R/U 30' conductor handling equipment. Observed 500 MT 12 ft bails did not fit into Weatherford 30' hydraulic elevators." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Held pre-job meeting for R/U 30' conductor handling equipment. Stopped the job and held Time Out For Safety (TOFS) as 500 MT 12 ft bails did not fit into Weatherford 30' hydraulic elevators. Evaluated situation and made new plan. Installed 80 MT shakles on 500 MT 12 ft bails and picked up elevator. Functioned tested open and close function on 30' elevators. Open and close function did not match controls on driller consolled. Attempted to change functions to match controls on drillers consol, NoGo." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Held TOFS and risk evaluated situation. Implement safety measures and held toolbox talk with relevant drilling personel." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held pre-job meeting with all involved prior to starting to run 30' conductor." "On 2013-03-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U 30' conductor shoe and set same in rotary table." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U first 30' intermediate joint and M/U same to 30' conductor shoe. Attempted to run in with 30' conductor. RIH connector 33.17' OD conductor stood up on Weatherford bushing in auto slips (32,5' ID). Evaluated situation and planned forward operation. Held toolbox talk with relevant personel due to changes in sequence of 30' conductor running operation." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Removed half moon bushing in Weatherford auto slips and run intermediate 30' joint connector below rotary table. Re-installed bushing and set conductor in auto slips." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 14m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Run 30' conductor to 14 m. Unable to pass weather deck split hatch." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 14m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Raised permit and conducted toolbox talk. Removed weather deck split hatch." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 24m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Removed bushing in Weatherford auto slips. Run 30' connector below rotary table to 24 m and re-installed bushing." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: M/U second 30' intermediate conductor joint. RIH 30' conductor from 24 m to 28 m. Flushed conductor with SW to function test floatshoe. RIH 30' conductor from 24 m to 36 m. At 02:51 hrs informed production 30' conductor shoe below centralizer deck and that production could start up on well F-14. Meanwhile ROV performed template survey." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 47m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Picked up and made up 30' conductor x-over joint. Removed half moon bushing in Weatherford auto slips and run 30' connector below rotary table. Re-installed bushing and set conductor in auto slips." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held pre-job meeting. Changed over handling equipment to 5 1/2' elevator." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held pre-job meeting. P/U 30' conductor housing on 5 1/2' handling tool." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: R/U handling equipment for making up 30' conductor well head housing." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held pre-job meeting. M/U 30' conductor housing with belt tong to 49 KNm and installed anti rotation locks and pins on same." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 51m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Removed half moon bushing in Weatherford auto slips and run connection between x-over joint and 30' connector housing below rotary table to 51 m. Re-installed bushing." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran down 30' conductor from 51 m through splash zone (MSL at ca. 54 m) to 61 m and filled 30' conductor with seawater. Observed significant movement of string (3 m significant wave hight). Evaluated situation - decision made to pull back above splash zone." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held Time Out For Safety meeting (TOFS). Checked with town connection OK. Formulated plan to limit time 30' conductor in splash zone to 52 m." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Removed 30' conductor lift tool on PRS. P/U 30' conductor running tool, installed 2' conductor fill up valve and inclinometer. M/U 3 doubles of fiberglass cement inner string and set back same in setdown area. Meanwhile: monitoring weather conditions. Sea Hz Sea max (m) (m) 11:00 3.0 4.8 12:00 2.4 4.0 13:00 2.4 3.9" "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Held pre-job meeting and observed seastate improved and safe to RIH 30' conductor through splash zone. Run 30' conductor down through splash zone from 52 m to 66 m continuosly observing proximity of 30' conductor string to adjacent production risers with ROV, 30' conductor did not make contact with same at any time. Filled 30' conductor with seawater." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: R/U C-plate for inner cementing string on top of 30' conductor housing and secured same. P/U and run fiberglass innerstring and secured in C-plate." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U 30' conductor running tool and M/U same to cementing innerstring. Removed C-plate and M/U 30' conductor running tool to 30' conductor housing. ROV engineer turned on inclinometer and checked same. Confirmed conductor fill-up ball valve open. Painted 'anti rotation' rotation line on running tool and conductor housing." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Picked up and removed 30' bowls. Installed battery in inclinometer and attempted to run through rotary. Snapped off 2' fill up valve. Evaluated situation and decided to installed handle on 2' fill up valve at moon pool level." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Run 30' conductor on 5 1/2' HWDP dedicated landing string from 93 m to above F-11 template funnel at 143 m." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Stabbed 30' conductor shoe into F-11 template funnel with ROV assistance. Held pre-job meeting evaluating risk of running in open hole riserless. Recorded Recorded Up/Down wt. 106/100 MT. RIH 30' conductor from 143 m to 36' TD at 202 m, recorded Up/Down weight 102/97 MT." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke circulation and observed with ROV seawater returns through 2' fill up valve on running tool, 400 lpm, 5 bar and closed same with ROV. ROV removed plug from F-12 30' conductor housing annulus cement return hole and verified F-11 setting depth. Digiquartz readings: Inclinometer: F-12(m) F-11(m) roll / pitch 86.887 86.832 0.02/0.10 86.835 86.842 0.01/0.11 86.872 86.828 0.03/0.12" "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Circulated 2.5 bottoms up with seawater, 2500 lpm, 15 bar. Meanwhile: Prepared for cementing operations" "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Held pre-job meeting with all involved personel prior to cement job. Notified production control room and engine room of up comming cement job. Meanwhile circulated 3 bottoms up, 2500 lpm, 15 bar." "On 2013-03-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Flushed cement line and verified cement line up with 20 bar. Leak tested cement line 100 bar / 5 min. Meanwhile: ROV positioned to observe top of 30' conductor housing and returns at seabed." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Mixed and pumped 60 m3, 1.55 sg Tuned Light XL cement, 700 lpm, 12 bar and displaced same inplace with 4.3 m3 SW, 1250 lpm of seawater, final circulating pressure 22.5 bar. Took bucket and cup samples of pumped cement slurry. Checked for back flow, broke off cement line and flushed same. Unable to observe cement returns at seabed with ROV while pumping same due to poor visibility. (Cement displaced completed at 01:51 hrs)" "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: ROV verified 30' conductor setting depth with Digiquartz hydrostatic depth measure and inclinometer roll / pitch readings. Final depth of top of 30' conductor housing= 140.1 mRKB. Note: F-12 top of 30' conductor housing 140.2 mRKB. Digiquartz readings: Inclinometer: F-12(m) F-11(m) roll / pitch 87.717 87.624 0.00/0.07 87.700 87.599 0.02/0.06 87 697 87.604 0.04/0.08" "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: Waiting on cement. Meanwhile: Visibility at template improved and ROV observed that cement was at seabed at 04:10 hrs. ROV checked 30' conductor setting depth. Digiquartz readings: Inclinometer: F-12(m) F-11(m) roll / pitch 87.117 87.055 0.01/0.07 87.175 87.033 0.01/0.07 87 179 87.035 0.00/0.06" "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'interruption -- wait' and lasted for 9.5 hours. Operational details: WOC, Meanwhile prepared to release 30' conductor running tool from 30' conductor and POOH running string." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held pre-job meeting with all personnel involved. ROV opened 2' fill up valve on top of 30' conductor running tool." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: With 1 ton tension on 5 1/2' HWDP running string. Released 30' conductor running tool with 5 right hand turns, 5 rpm, 1-2 KNm and POOH with inner cement string from 192 m to below top of 30' conductor to 150 m." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Flushed 4 3/4' inner cement string, 3400 lpm, 20 bar. Observed by ROV POOH running string and cement inner string from 150 m to 56 m. Removed master bushing and POOH to 50 m and re-installed master bushing." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: R/U false rotary. B/O 30' conductor running tool and 5 1/2' HWDP running string and, B/O and L/D 4 3/4' inner cement string." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held pre-job meeting. B/O 30' conductor running tool 5 1/2' HWDP L/O same. Picked up 5 1/2' HWDP double to M/U stand for dedicated landing string, racked back same." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Prepared for cutting transport system (CTS) funnel and hose." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Held pre-job meeting. P/U and run CTS funnel on tugger from moon pool and installed same on 30' conductor housing observed by ROV. Meanwhile: Leak tested top drive wash pipe to 100 bar / 5 min." "On 2013-03-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: P/U and run CTS 40 m hose on tugger from moon pool observed by ROV." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Run cuttings transport system (CTS) hose connected same to CTS funnel. Meanwhile: Prepared for M/U 26' BHA." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: Held pre-job safety meeting prior to picking up 26' BHA. P/U and M/U mud motor steerable BHA with OnTrak tool and 26' bit and RIH same to 26 m. Adjusted bend on mud motor housing to 1,00 deg." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- trip' and lasted for 7.0 hours. Operational details: P/U and M/U GyroTrak tool and BHA, RIH from 26 m to 103 m observing with ROV below splash zone." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 131m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH 26' BHA on 5 1/2' HWDP from 103 m to 131 m. Observed by ROV." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 131m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: ROV verified CTS operational." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH 26' BHA on 5 1/2' HWDP from 131 m. Stabbed into CTS with ROV assistance and RIH to 145 m. Meanwhile: P/U 20' casing from spud boat and L/O same on cantilever deck." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: R/U wire line equipment prior to up coming Gyro single shot runs." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 172m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 26' BHA on 5 1/2' HWDP from 145 m to 172 m. Meanwhile: P/U 20' casing from spud boat and L/O same on cantilever deck." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Washed down from 172 m and tagged firm cement at 197 m with 4-5 MT, 40 rpm, 1-2 KNm, 3400 lpm, 85 bar." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Established drilling parameters and drilled out shoetrack to 202 m, 40 rpm, 2-3 KNm, 4500 lpm, 130 bar, WOB 1-2 MT. Pumping regular hivis sweeps. Meanwhile: Held toolbox talk with Wireline, Gyro, Deck personnel and crane driver regarding safe coordination of wireline operations and casing operations on canilever deck. P/U 20' casing from spud boat and L/O same on cantilever deck." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and cleaned out rathole in 1-2 m steps from 202 m to 208 m, 40 rpm, 1-2 KNm, 4400 lpm, 128 bar. Meanwhile: P/U 20' casing from spud boat and L/O same on cantilever deck." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 208m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Reamed rathole 3 times, 40 rpm, 1-2 KNm, 4400 lpm, 128 bar. No restriction or excess drag/ torque observed. Meanwhile: P/U 20' casing from spud boat and L/O same on cantilever deck." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pulled through rat hole and shoetrack to 197 m and verified no restrictions, 0 rpm, 0 lpm. Meanwhile: P/U 20' casing from spud boat and L/O same on cantilever deck. Held pre-job meeting prior to performing single shot Gyro run." "On 2013-03-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Ran wireline gyro single shot survey. Gyro Survey: (mRKB) (deg.) 167.7 0.29 147.7 0.21" "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: POOH with wireline gyro." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 210m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Drilled 26' hole from bottom of rat hole at 208 m to 210 m, 4470 lpm, 133 bar, 60 rpm, 2-3 KNm. Made several attempts to take survey with MWD -No Go." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 213m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 26' hole from 210 m to 215 m, 4450 lpm, 132 bar, 90 rpm, 6-9KNm. At 1:15hrs while drilling 26' hole at 215 m one half (5 kg) of a 2 piece Top Drive Pipe Handler Stabbing Guide and three (3 x 200 grm) of the seven bolts securing same to Top Drive fell down 8 m from the top dive to the drill floor." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 213m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Impact of the dropped 5kg part of the stabbing guide was estimated as 400 joules. Barriers were in place at the rig floor, no personal were on the rig floor, and the objects fell down within the Red Zone. No personnel injury took place. Notification was given to Statoil and MDN offshore and onshore management. Picked up off bottom from 215 m to to 213 m and held TIme Out For Safety (TOFS) meeting." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 213m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Evaluated situation and formulated forward plan." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 213m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Held pre-job meeting. Prepared permits and isolated drilling equipment on drill floor. Used work basket to inspect Top drive." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 184m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Pulled back 26' BHA from 213 m to inside 30' conductor shoe at 202 m to 184 m. Racked back one 5 1/2' DP stand." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 184m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Lowered top drive to rig floor inspected same. Recorded details of dropped object incident. Re-installed Pipe Handler Stabbing Guide onto Top drive." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 185m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: M/U 5 1/2' DP stand and attempted to test communication to MWD tools, no go." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 224m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 26 hole from 215 m to 224 m,4500 lpm, 147 bar, 60 rpm, 3-6 KNm, Gross ROP: 11 m/hr, WOB 1-2 MT. Evaluated situation and prepared to POOH. Meanwhile: Baker discussed MWD operational problems with onshore support and reported the MWD tool failure mode to be a 'De-Sync' failure that would not be possible to solve with the MWD tools in hole. Prepared to inspect drilling equipment in derrick prior to POOH 26' BHA to change out MWD tools." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 224m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Performed full derick and equipment inspection prior to POOH. Meanwhile: Mixed 1.40 sg mud." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 144m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Displaced well with 30 m3, 1.40 sg mud, 2500 lpm, 40 bar, 10 rpm, 1-2 KNm. POOH from botton at 224 m to 144 m." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 144m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Topped up well with 10 m3, 1.40 sg mud, 2000 lpm, 40 bar." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 144m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Waited on prodution to complete shuting-in wells." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: At 12;06hrs Production confirmed wells F-7, F-12 and F-14 shut-in. POOH 26' BHA from CTS funnel at 144 m to 37 m, observed by ROV." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Chanded handling equipment. POOH 26' BHA and inspected bit, observed no indication of junk in hole." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 22m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: RIH 26' motor steerable BHA to 32 m and resumed braking down same to 22 m. GyroTrack tested and found to be re-runable" "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 22m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Seal ring between top of OnTrack and modular stabilizer observed to be out of position. Directional Driller advised that this could be caused by a leaking and/or exploded lithium battery within the OnTrak tool, with risk of personal being exposure to toxic gas and liquids. All personnel were immediately moved off the drill floor to a safe area in the dog house. Barriered off rig floor. Evaluated situation Baker discussed with onshore HSE organisation. Informed offshore and onshore management." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 22m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Performed SJA meeting and formulated plan with involvement of Baker onshore organization and technical management." "On 2013-03-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Prepared permits and held pre-job/SJA meeting with all involved personal." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 22m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Baker took temperature and gas measurements to evaluate the possibility of damage and leakage from the lithium batteries inside the OnTrack. Temperature and gas reading indicated OnTrack Lithium batteries intact. Changed out fox hole inserts. P/U back up OnTrack and placed same in fox hole. B/O handling sub on back up OnTrack." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 22m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: M/U lifting sub to failed Ontrack tool using PRS and iron roughneck, no personal on drill floor." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 13m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH from 22 m to 13 m. B/O OnTrack below NM Stop Sub. With the lifting sub in place above and the NM Stop Sub inplace below the Lithium batteries were effectively sealed inplace within the OnTrack tool. L/O OnTrack and verified tool still intact with temperature and gas measurements." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: P/U and M/U back up OnTrack. POOH and painted bit." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: P/U and M/U 26' motor steerable BHA. Connected up to MWD tool and started testing same." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Troubleshoot connection on MWD tools, faulty cable." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 131m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: M/U 26' BHA and RIH from 21 m through splash zone to 131 m, observed with ROV." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RIH from 131 m to template and stabbed 26' into CTS funnel to 142 m, observed by ROV." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 224m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH from 142 to 171 m. Washed down from 171 to m through 30' conductor shoe at 202 m to bottom at 224 m, 1000 lpm, 30 bar." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 262m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 26' hole from 224 m to 262 m, 4500 lpm, 155 bar, 80 rpm, 7-12 KNm, WOB 2-3 MT, Gross ROP 6 m/hr. Pumping 10 m3 Hi-vis sweeps every single and took OnTrack surveys." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 282m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 26' hole from 262 m to 282 m, 4500 lpm, 154 bar, 80 rpm, 6-9 KNm, WOB 1-2 MT, Gross ROP 5 m/hr. Pumping 8 m3 Hi-vis sweeps every single and took OnTrack surveys." "On 2013-03-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 282m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Evaluated survey data." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 282m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Evaluated survey data, well path and forward plan with town." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Picked up off bottom at 282 m and racked back stand. Reamed 26' hole from 212 m to 250 m, 3500 lpm, 103 bar, 40 rpm, 4-6 KNm" "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Inspected Top drive." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Racked back one 5 1/2' DP stand. R/U wireline lower sheave and ran gyro down to UBHO sub. Orientated string to 27 deg to give optimum well path direction. POOH Gyro and R/D wireline." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 207m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Reamed orientated below 30' conductor shoe at 202 m to 207 m, 4500 lpm, 148 bar." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 211m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Reamed orientated below 30' conductor shoe at 202 m to 211 m, 4500 lpm, 148 bar." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 199m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Observed leak on top drive IBOP. Pulled back into 30' conductor shoe at 202 m to 199 m. Lowered Top drive to rig floor. Held Time Out For Safety (TOFS). Isolated Top drive, removed leaking actuator cylinder on IBOP and isolated hydraulic hoses. Meanwhile: Perform derrick inspection and checks due to high wind speed." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 251m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: RIH from 199 m reamed inside 30' conductor shoe and orientated reamed from 207 m to 251 m, 4500 lpm, 146 bar, WOB 0.5-1 MT." "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 229m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Pulled back from 251 m to 229 m recording MWD OnTrack inclination survey data. Inclination Survey (OnTrack): Survey station (m) Inclination (deg) 231 0.22 221 0.44 211 0.03" "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 266m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Evaluated new survey data after orienated reaming and discussed same with town. Agreed plan to proceed with orientated reaming lower part of 26' openhole. Reamed orientated from 251 m to 266 m, 4500 lpm, 147 bar, WOB 0-1 MT and recorded MWD OnTrack survey data. Inclination Survey: Survey station (m) Inclination (deg) 231 0.24 221 0.31" "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 281m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Reamed orientated from 266 m to 281 m, 4500 lpm, 148 bar, WOB 0-1 MT" "On 2013-03-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 281m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Pulled back to 250 m and reamed orientated to 281 m, 4500 lpm, 148 bar, WOB 0-1 MT" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Recorded MWD OnTrack inclination survey data while pulling back from 281 m to 250 m. Inclination Survey (OnTrack): Survey station (m) Inclination (deg) 261 0.90 251 0.67 231 0.58" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Racked back 5 1/2' DP stand. Inspected Top drive and Travelling block. Meanwhile: Held DOP meeting." "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 279m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: B/O and L/D 5 1/2' DP single. R/U and ran wireline gyro. Orientated tool face and POOH recording wireline gyro surveys. R/D wireline lower sheave. Re-calculated projected well path. Wireline Gyro Inclination Survey: Survey station (m) Inclination (deg) Azi (deg) 239 0.49 217.49 228 0.48 202.49 218 0.25 195.59 208 0.21 181.56 202 0.26 233.95" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 292m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Established drilling parameters. Orientated drilled 26' hole from bottom at 281 m to 292 m and recorded OnTrack survey data. Unable to record GyroTrack Survey data. Inclination Survey (OnTrack): Survey station (m) Inclination (deg) 270 0.85" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 292m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline lower sheave and ran wireline gyro." "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 292m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Verified 26' mud motor toolface and recorded wireline single shoot survey. Re-calculated projected well path. Wireline Gyro Inclination Survey: Survey station (m) Inclination (deg) Azi (deg) 251.3 0.57 204.82" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 301m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Orientated drilled 26' hole from bottom at 292 m to 301 m and recorded OnTrack survey data. Re-calculated projected well path. Inclination Survey (OnTrack): Survey station (m) Inclination (deg) 289 0.85" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 306m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Orientated drilled 26' hole from bottom at 301 m to 306 m." "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 306m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: R/U wireline lower sheave, ran wireline gyro and recorded wireline single shoot survey. Re-calculated projected well path. Wireline Gyro Inclination Survey: Survey station (m) Inclination (deg) Azi (deg) 261.3 0.6 167.13" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 320m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Orientated drilled 26' hole from bottom at 306 m to 320 m and recorded OnTrack survey data. Re-calculated projected well path. Inclination Survey (OnTrack): Survey station (m) Inclination (deg) Azi (deg) 300.00 0.53 135" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 318m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Picked up off bottom at 320 m to 318 m. B/O 5 1/2' DP single and R/U wireline lower sheave. Ran wireline gyro and recorded wireline single shoot survey. Re-calculated projected well path. Wireline Gyro Inclination Survey: Survey station (m) Inclination (deg) Azi (deg) 278.3 0.56 198.61" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 332m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Orientated drilled 26' hole from bottom at 320 m to 332 m and recorded OnTrack survey data. Re-calculated projected well path. Inclination Survey (OnTrack): Survey station (m) Inclination (deg) Azi (deg) 312.37 0.77 186" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 332m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline lower sheave, ran wireline gyro and recorded wireline single shoot survey. Re-calculated projected well path. Wireline Gyro Inclination Survey: Survey station (m) Inclination (deg) Azi (deg) 291.7 0.57 185" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 332m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Evaluated survey data and projected well path and discussed same with town Meanwhile: R/U and ran down tugger from moon pool to tension deck to enable 5 1/2' DP drill string to be pulled securely against slot opening in tension deck to reduce string movement and attempt to take GyroTrack survey." "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 332m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Tagged bottom at 332 m and recorded OnTrack/GyroTrack survey data while securing 5 1/2' DP drill string in moon pool and at tension deck. Re-calculated projected well path. Inclination Survey (OnTrack/GyroTrack): Survey station (m) Inclination (deg) Azi (deg) OTR/GRT OTR/GRT OTR/GRT 312.00 /304.10 0.77 /0.52 185.07 /245.99 312.00 /304.10 0.77 /0.70 182.41 /199.93 312.21 /304.22 0.80 /0.62 FAIL /175.68 312.04 /304.05 0.77 /0.70 FAIL /113.45" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 347m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Orientated drilled 26' hole from bottom at 332 m to 347 m and recorded OnTrack/GyroTrack survey data. Re-calculated projected well path. Inclination Survey (OnTrack/GyroTrack): Survey station (m) Inclination (deg) Azi (deg) OTR/GRT OTR/GRT OTR/GRT 327.21 /319.22 0.58 /0.70 FAIL /194.06" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 347m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: R/U wireline lower sheave, ran wireline gyro and recorded wireline single shoot survey. Re-calculated projected well path. Discussed survey data and projected well path with town. Decision made to plug back 26' open hole from bottom at 347 m to 30' conductor shoe at 202 m, run alternative 26' BHA configuration mud motor assembly and kick off below 30' conductor shoe. Wireline Gyro Inclination Survey: Survey station (m) Inclination (deg) Azi (deg) 301.7 0.58 167 305.5 0.68 162" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 347m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Circulated hole clean, 3500 lpm, 93 bar. Displaced well with 60 m3, 1.35 sg spud mud, 4000 lpm, 115 bar. 3 hrs advance notice given to Production to shut-in well F-14" "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: POOH 26' BHA from bottom at 347 m inside 30' conductor at 202 m to 142 m." "On 2013-03-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Isolated rig floor equipment. R/D Wireline equipment and inspected top drive and travelling block." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Inspected top drive and traveling block. Found significant wear on top drive torque back-up clamp torque arrestor." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 132m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH 26' BHA on 5 1/2' HWDP from 142 m to 132 m and racked back same." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.5 hours. Operational details: Production confirmed well F-14 shut-in at 02:40 hrs. POOH 26' BHA from 132 m to 14 m breaking down 26' BHA, racked back and L/O same." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Dumped MWD data." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Unable to rack back MWD tools due to PRS unable to handle non-mag. RIH w/ on-track to 20 m." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Performed tool box talk, L/D and racked 26' BHA." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Cleared and cleaned drill floor." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 169m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Picked up, made up and RIH with 5 1/2' DP cement stinger with 5' diverter sub." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 169m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: Performed tool box talk and repaired worn components on top drive." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 331m. The activity was categorized as 'interruption -- repair' and lasted for 5.5 hours. Operational details: RIH cement stinger observing with ROV in water, entered F-11 template slot, RIH to 231 m and took 2 tons down weight. Attempted to rotate string with pipe handler to work past restriction area. No-go, engaged top drive and rotated with 10 rpm and 3000 l/min, 4 bar. No-go. Increased rotation to 40 rpm and flow to 4000 l/min, 12 bar. Worked string pasted obstruction and continued washing cement stinger to 331 m." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 347m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH w/ cement stinger on 5 1/2' DP from 331 m, 1000 l/min, 4 bars and tagged TD @347 m with 2 tons. Picked off bottom and circulated 2 x bottoms up with 4000 l/min, 15 bar, 25 rpm, 1-2 kNm." "On 2013-03-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 345m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Racked back stand and M/U cement stand. RIH to 345 m on cement stand." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 345m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: M/U side entry sub and cement hose. Attempted to flush line from cement unit, observed pressure build up to 35 bar. Bled off pressure, disconnected cement line and confirmed not blocked. Attempted to flush string with rig pumps, observed pressure build up to 25 bar. Bled off pressure and R/B cement stand, engaged top drive, applied 90 bar and picked up to 318 m. Observed pressure dropping to 0 bar, increased flow to 4000 l/min, 15 bar and flushed through cementing string." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 345m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: M/U cement stand and RIH to 2 m off bottom at 345 m w/1000 l/min, 5 bar. Connected and tested cement line, 20/100 bar for 5/10 min." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 345m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Mixed and pumped 78 m3 of 1.92 SG G neat cement slurry. Displaced cement with 2.1 m3 sea water with cement unit." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 331m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Pulled out with cement stand and attempted to rack back same, forward PRS failed. Attempted to use PRS over-ride function, no-go. Unable to use aft PRS. Trouble shoot and made continancy plan of POOH cement stinger in single 5 1/2' DP joints. Re-established operation of forward PRS." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 195m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH cement stinger at 3 min/stand to inside 30' shoe at 202 m to 195 m. Circulated 2 x bottoms up 4000 l/min, 8 bar, 30 rpm, 1-2 kNm." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: POOH to above seabed at 100 m, inserted 2 x sponge balls and circulated string clean, 4000 l/min. POOH to surface observed by ROV." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Performed tool box talk and L/D X-over and cement stinger." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 9.5 hours. Operational details: Waited on cement. Meanwhile: changed encoder on aft PRS. Performed maintenance on top drive and trouble shoot alignment on same. Calibrated aft PRS and prepared to run 26' BHA." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Confirmed with Production that wells adjacent to F-11 shut in. Performed Pre-job Meeting prior to M/U 26' steering BHA." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: P/U string stab and prepared rig tongs." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting with newly arrived night drill crew prior to M/U 26' steering BHA." "On 2013-03-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- repair' and lasted for 4.5 hours. Operational details: P/U and M/U 26' steering BHA to 37 m. Transferred scribe line from motor bent sub to UBHO and uploaded data to MWD." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: P/U and M/U 26' BHA, activated Gyro Trac and checked scribe line." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: L/D X-over and 1 x single joint HWDP. M/U lifting nipple and plugged into MWD, tilted string to verify Gyro function. Disconnected cable and RIH with 26' steering BHA to 37 m." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: M/U and RIH 26' steering BHA from 37 m through splash zone to template observed by ROV. Stabbed into well funnel and RIH to 155 m ." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- repair' and lasted for 4.5 hours. Operational details: Changed out top drive alignment cylinder." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: M/U 5 1/2' HWDP stand and recorded parameters." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Performed Pre-job, safety and DOP Meeting prior to washing down to find TOC and dress off same to firm cement for kick off." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 202m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Washed down with 26' steering assembly in 30' conductor from 155 m to shoe at 202 m, 1000 l/min, 8 bar, 15 rpm, 2 kNm. Had no indication of cement in shoe track." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 230m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Washed down with 26' steering assembly from 202 m to 230 pulling back into shoe every 5 m to check BHA free, 500 l/min, 7 bar. Had no indication of cement in rat hole or 26' open hole." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 244m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Washed down with 26' steering assembly from 230 m to 244 m, 500 l/min, 7 bar, 15 rpm, 2 kNm. Took 5 tons down weight indicating TOC. Pumped 10 m3 Hi-Vis pill and circulated hole clean, 1000 l/min, 8 bar." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 244m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Performed tool box talk, R/U wireline, took survey and oriented string prior to drilling ahead in steering mode." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 246m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Washed down in orienting mode from 244 m to 246 m, 2380 l/min, 45 bar, 0 tons WOB. At 246 m set down 5 tons WOB and had indications of firm cement. Started time drilling from 246 m." "On 2013-03-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Oriented time drilled 26' hole from 246 m to 250 m, 3080 l/min, 75 bar, 1 - 2 tons WOB, 2 m/hrs. Pumped Hi-vis sweeps." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 251m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Oriented time drilled 26' hole from 250 m to 251 m. 3080 l/min, 75 bar, 1 - 2 tons WOB, 2 m/hrs. Pumped Hi-vis sweeps as required." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 251m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (251 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 209 0.25 232.83" "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 257m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Oriented time drilled 26' hole from 251 m to 257 m. 3080 l/min, 75 bar, 1 - 2 tons WOB, 2 m/hrs. Pumped Hi-vis sweeps. Transferred over to well 15/9-F-11 T2" "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 266m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Transferred over from well 15/9-F-11. Oriented time drilled 26' hole from 257 m to 266 m, 3080 l/min, 75 bar, 1 - 2 tons WOB, 2 m/hrs. Pumped Hi-vis sweeps." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 266m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Attempted to take MWD Gyro trac survey, no-go." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 266m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Attempted to L/D single 5 1/2' DP joint to prior to taking wirelien Gyro survey. P/U with 30 tons overpull and pulled free. Pumped Hi-vis sweep and circulated same out of hole. Increased flow to 4100 l/min, 130 bar and worked string over interval 237 m to 244 m." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 238m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Made wiper trip from 244 m to inside 30' shoe at 202 m with 3000 l/min, 72 bar, 15 RPM, 2 kNm." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 244m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Washed and reamed down from 30' Conductor shoe at 202 m to 244 m, 3000 l/min, 72 bar, 15 RPM, 2 kNm, no obstruction observed. Reamed back from 244 m to 238 m, 3000 l/min, 72 bar, 15 RPM, 2 kNm." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 238m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (238 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 196 0.14 241.85" "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 266m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Washed down from 238 m to bottom at 266 m, 3000 - 3500 l/min, 72 - 90 bar. No obstruction observed." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 265m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (265 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 223.6 0.58 285.5" "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 279m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Oriented toolface, POOH and R/D wireline. Oriented time drilled 26' hole from 266 m to 272 m, 3460 l/min, 98 bar, 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 279m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Evaluated directional data. Drilled 26' hole from 272 m to 279 m, 3460 l/min, 98 bar, 40 RPM, 5 kNm, 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 279m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (277 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 236.9 0.59 283.17" "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 292m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Drilled 26 hole from 279 m to 292 m, 3670 l/min, 110 bar, 40 RPM, 5 kNm, 2 - 5 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 292m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (290 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 249.0 0.97 314.87" "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 306m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Drilled 26 hole from 292 m to 306 m, 3670 l/min, 110 bar, 40 RPM, 4 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 306m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (305 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 264.0 1.32 310.50" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 318m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Drilled 26' hole from 306 m to 318 m, 3650 l/min, 105 bar, 40 RPM, 5 kNm, 2 - 5 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 318m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (317 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 276.4 1.41 316.92" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 333m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Drilled 26' hole from 318 m to 333 m, 3650 l/min, 105 bar, 40 RPM, 5 kNm, 2 - 5 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 333m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (332 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 290.2 1.30 318.66" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 346m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Drilled 26' hole from 333 m to 346 m, 3760 l/min, 110 bar, 40 RPM, 5 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 346m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (345 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 305 1.06 321.43" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 359m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 26' hole from 346 m to 359 m, 3760 l/min, 110 bar, 40 RPM, 5 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 359m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: R/U wireline, RIH and took Gyro survey (358 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 317.0 0.98 327.19" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 374m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 26' hole from 359 m to 374 m, 3760 l/min, 110 bar, 40 RPM, 5 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 374m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (373 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 332.0 1.08 321.81" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 387m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 26' hole from 374 m to 387 m, 4400 l/min, 155 bar, 40 RPM, 5 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 387m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Attempted to take MWD survey, no-go. R/U wireline, RIH and took Gyro survey (386 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 344.7 1.07 325.46" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 402m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 26' hole from 387 m to 402 m, 4500 l/min, 155 bar, 40 RPM, 5 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 402m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Attempted to take MWD survey, no-go. R/U wireline, RIH and took Gyro survey (401 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 358.2 1.13 318.40" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 414m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Orient drilled 26' hole from 387 m to 402 m, 4500 l/min, 155 bar, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 414m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: R/U wireline, RIH and took Gyro survey (413 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 371.7 1.16 320.72" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 428m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Orient drilled 26' hole from 414 m to 421 m, 4500 l/min, 155 bar, 2 - 4 tons WOB. Started rotation, 40 RPM, 4 kNm and continued drilling 26' hole from 421 m to 428 m, 4500 l/min, 155 bar, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 428m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Attempted to take MWD survey, no-go. R/U wireline, RIH and took Gyro survey (427 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 385.0 1.40 317.81" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 441m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 26' hole from 428 m to 441 m, 3500 - 4500 l/min, 70 - 155 bar, 40 RPM, 5 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 441m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Attempted to take MWD survey, no-go. R/U wireline, RIH and took Gyro survey (440 m bit depth): Survey station (m) Inclination (deg) Azi (deg) 398.2 1.78 319.73" "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 454m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 26' hole from 428 m to 441 m, 4500 l/min, 155 bar, 40 RPM, 5 kNm, 2 - 4 tons WOB. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 454m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Attempted to take MWD survey, no-go. Detected unusual noise from crown block fast-line sheave." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 454m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Checked crown block fast-line sheave and found bearing ceased onto shaft. Evaluated situation and informed offshore and onshore managment. Prepared forward plan to POOH 26' BHA prior to working on fast-line sheave. Barriered off rig floor and cantelever. Meanwhile: Circulated well 1100 l/min, 8 bar, 20 RPM, 2 kNm. Attempted to apply lubricant to fast-line sheave." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 454m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Performed Pre-job Meeting held SJA on drill floor prior to POOH. Meanwhile: Circulated well 1100 l/min, 8 bar, 20 RPM, 2 kNm. Pumped Hi-vis sweeps." "On 2013-03-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 454m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Prepared POOH from 453 m to surface. Installed grease pump in crown block. Transferred 1.35 sg KCl mud to active. Rigged down wireline equipment. Meanwhile: Circulated well 1100 l/min, 8 bar, 20 RPM, 2 kNm. Pumped Hi-vis sweeps." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 438m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Prepared POOH from bottom at 453 m. Installed grease pump in crown block. Oriented 26' steering BHA. Displaced well to 1.35 sg KCl mud, 1100 - 3100 l/min, 8 - 70 bar. Confirmed barriered off rig floor and cantelever. POOH from 454 m, recorded overpull of 30 tons. Broke circulation 650 l/min, 10 bar, 40 RPM, 15 kNm. POOH up through tight spot from 454 to 438 m. Stand of 5 1/2' DP mistakenly released from elevators while still connected in rotary." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 438m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Connected PRS to 5 1/2' DP stand in derrick and connected elevators to same." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 128m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: POOH 26' BHA on 5 1/2' DP from 438 m and above seabed at 144 m to 128 m observed by ROV." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 100m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: R/B 26' BHA from 128 m to 100 m." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 100m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting with new crew prior to handling 26' BHA." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: R/B 26' BHA from 100 m to 37 m." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting prior to L/D 26' BHA to deck." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Dumped MWD data and L/D 26' BHA to deck." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting prior to preparing for changing out fast-line sheave in crown block." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 7.0 hours. Operational details: Prepared for changing out fast-line sheave in crown block. Visually inspected top drive, hung off top drive, rigged down wireline equipment." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to work aloft on fast-line sheave in crown block." "On 2013-03-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Waited on flair prior to work aloft. Meanwhile: Made tools ready to work on fast-line sheave in crown block, cleared and cleaned rig floor, prepared BOP test stump and performed general rig maintenance." "On 2013-03-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 7.0 hours. Operational details: Prepared for changing out fast-line sheave in crown block. Transferred tools to derrick. Meanwhile: Performed general rig maintenance." "On 2013-03-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to work aloft on fast-line sheave in crown block." "On 2013-03-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 11.5 hours. Operational details: Prepared for changing out fast-line sheave in crown block. Transferred high-torque tools to derrick. Loosened all bolts on sheave and secured same in derrick. Meanwhile: Performed general rig maintenance, changed wires on overhead cranes, detected leakage on BOP annular function and trouble shoot same." "On 2013-03-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to work aloft on fast-line sheave in crown block." "On 2013-03-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 4.5 hours. Operational details: Prepared for transferring fast-line sheave from derrick to drill floor. Meanwhile: Performed general rig maintenance, trouble shoot leakage on BOP annular function." "On 2013-03-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 6.0 hours. Operational details: Transferred fast-line sheave from derrick to drill floor, and lifted same from rig floor to welders workshop. Meanwhile: Performed general rig maintenance, trouble shoot leakage on BOP annular function." "On 2013-03-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 8.0 hours. Operational details: Repaired failed fast line sheave and re-assembled bearing assembly. Meanwhile: Performed service and visual inspection of forward and aft Pipe Racking System. Continued BOP annular repair. Tested backup MWD tools. Serviced TDS travelling block and dolly. Repaired TDS hangoff wire." "On 2013-03-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Transferred fast-line sheave to rig floor. Prepared sheave for transport to crown block." "On 2013-03-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Performed toolbox talk prior to hoisting fast-line sheave to crown." "On 2013-03-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 9.0 hours. Operational details: Transferred fast-line sheave from drill floor to derrick. Installed sheave. Meanwhile: Performed general rig maintenance, trouble shoot leakage on BOP annular function." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 7.0 hours. Operational details: Continued installing fast-line sheave in derrick. Meanwhile: Repaired leakage on BOP annular function. Prepared to function test same." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Performed prejob meeting prior to rig down lifting gear and equipment from derrick." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 4.5 hours. Operational details: Transfered equipment from derrick to rig floor and rigged down lifting equipment. Performed derrick inspection. Calibrated crown grease pump. Ran drawworks and confirmed sheave movement." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Rigged up wireline sheave." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Picked up and made up 26' bottom hole assembly to 10m." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 10m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Waiting for stop of production on well F-14/F-12. Meanwhile: Performed general maintenance." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- repair' and lasted for 7.8 hours. Operational details: Picked up and made up 26' bottom hole assembly to 140m." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 152m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Stung 26' bit into conductor housing funnel and ran in hole with 26' bottom hole assembly from 140m MD to 152m MD. Informed production supervisor - ready to start up F-14 production." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 152m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting prior to run in hole with 26' bottom hole assembly. Meanwhile: Ran wireline gyro and set to 356 degrees." "On 2013-03-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 230m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Ran in hole with 26' bottom hole assembly on 5 1/2' drill pipe from 152m MD to 230m MD." "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 406m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Ran in hole with 26' bottom hole assembly on 5 1/2' drill pipe from 230m MD to 406m MD. Observed resistance at 406m MD. Attempted to pass restriction with 10MT - no go." "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 454m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Established circulation with 2000 lpm and 30 bar. Attempted to pass restriction with 2000 lpm and 30 bar - no go. Increased flow to 3000 lpm and 90 bar. Washed in hole with 26' bottom hole assembly on 5 1/2' drill pipe with 3000 lpm and 90 bar from 406m MD to 454m MD. Tagged bottom with 10 MT." "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 454m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed survey with GyroTrak. Survey station (m) Inclination (deg) Azi (deg) 426.7 2.55 313.14" "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 469m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 26' hole from 454m MD to 469m MD with 4500 lpm, 152 bar, 1.12 sg ECD, 40 surface RPM (130 total RPM), 4-9 kNm, 2-8 MT. Pumped 10m3 hi-visc pill for every single. Average ROP: 12 m/hr. Performed survey with GyroTrak. Survey station (m) Inclination (deg) Azi (deg) 444.6 2.46 316.30" "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 646m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled 26' hole from 469m MD to 639m MD with 4500 lpm, 152-162 bar, 1.12-1.14 sg ECD, 40-60 surface RPM (130-150 total RPM), 4-12 kNm, 2-15 MT. Pumped 10m3 hi-visc pill for every single. Gyro performed every stand. Average ROP: 17.9 m/hr" "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 650m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Slided and oriented 26' hole from 639m MD to 650m MD with 4500 lpm, 162-165 bar, 1.12 sg ECD, 5-10MT. Average ROP: 11 m/hr" "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 674m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 26' hole from 650m MD to 674m MD with 4500 lpm, 162-163 bar, 1.12 sg ECD, 60 surface RPM (150 total RPM), 6-9 kNm, 6-15 MT. Pumped 10m3 hi-visc pill for every single. Average ROP: 16 m/hr" "On 2013-03-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 793m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled and oriented 26' hole from 674m MD to 793m MD with 4500 lpm, 162-168 bar, 1.12-1.14 sg ECD, 60 surface RPM (150 total RPM), 6-13 kNm, 5-17MT. Pumped 10m3 hi-visc pill for every single. Average ROP: 14.9 m/hr" "On 2013-03-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 850m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Slided and oriented 26' hole from 793m MD to 850m MD with 4500 lpm, 152-163 bar, 1.09-1.10 sg ECD, 8-20MT. Pumped 10m3 hi-visc pill for every single. Average ROP: 9,5 m/hr" "On 2013-03-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 885m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Slided and oriented 26' hole prior to entering Utsira formation from 850m MD to 885m MD with 4500 lpm, 163-174 bar, 1.09-1.13 sg ECD, 7-20MT. Pumped 10m3 hi-visc pill for every single. Average ROP: 10 m/hr Entered Utsira Fm at 885m MD." "On 2013-03-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1071m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled and oriented 26' hole from 885m MD to 1071m MD with 3000 lpm, 88-94 bar, 1.13-1.16 sg ECD, 30 surface RPM (120 total RPM), 3-14 kNm, 4-15 MT. Observed occational hard stringers. Pumped 10m3 hi-visc pill for every single. Average ROP: 19.6 m/hr Base Utsira Fm at 1071m MD." "On 2013-03-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1102m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Slided and oriented 26' hole from 1071m MD to 1102m MD with 4500 lpm, 171-176 bar, 1.09-1-13 sg ECD, 15-20 MT. Observed sticky formation and problems maintaining toolface. Pumped 10m3 hi-visc pill for every single. Reamed every stand prior to taking connection. Average ROP: 6.2 m/hr" "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1359m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Slided and oriented 26' hole from 1345m MD to 1359m MD with 4500 lpm, 171-175 bar, 1.09-1.10 sg ECD, 12-18 MT. Pumped 10m3 hi-visc pill for every single. Reamed every stand prior to taking connection. Average ROP: 7.0 m/hr" "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1365m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Slided and oriented 26' hole from 1359m MD to 1365m MD with 4500 lpm, 171-176 bar, 1.09-1.10 sg ECD, 12-18 MT. Observed hard formation. Base Skade Fm verified to 1330m MD. Section TD set to 1365m MD. Average ROP: 4.5 m/hr" "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1365m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 6.0 hours. Operational details: Circulated hole clean with 4500-4800 lpm, 172-196 bar and 80 RPM. Pumped 2 x 30m3 hi-visc sweeps and circulated 3 x bottoms up." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1365m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Ran in hole and tagged TD with 5MT. Displaced open hole volume with 1.35 sg KCl mud at 4800 lpm, 195 bar and 80 rpm. Observed problems with suction on mud pumps." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 1365m MD to 460m MD. Observed tight hole at 460m MD. Attempted to get past restriction with maximum 30MT overpull - no go." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Established circulation with KCl mud at 500 lpm. Attempted to lubricate out of hole with 26' bottom hole assembly with 500 lpm and 10 rpm - no go." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Established circulation with seawater at 4000 lpm, 170 bar and 30 rpm. Reamed stand from 472m MD to 432m MD. Continued to circulate hole clean with 4000 lpm, 170-175 bar and 30 rpm. Circulation interupted by mud pumps shutting down." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 460m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Troubleshoot and repaired eletrical fault on mud pumps. Meanwhile: Pulled out of hole with 26' bottom hole assembly from 460m MD to 350m MD to check hole conditions. No overpull observed." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Ran in hole with 26' bottom hole assembly from 350m MD to 460m MD." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Displaced remaining open hole volume with 1.35 sg KCl mud at 4000 lpm, 10 rpm." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 185m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 460m MD to 185m MD. Informed Production Control Room to shut down producing wells according to SIMOPS." "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 185m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: Performed scheduled service on top drive and pipe racking system. Performed pre-job meeting prior to lay down / rack back 26' bottom hole assembly. Meanwhile: Shut down producing wells (F-12 and F-14)" "On 2013-04-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Racked back 5 1/2' heavy weight drill pipe in derrick from 185m MD to 144m MD." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Broke out and racked back 5 1/2' heavy weight drill pipe and 9 1/2' drill collars in derrick from 144m MD to 60m MD." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Downloaded MWD." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: Broke out and laid down OnTrak, GyroTrak and motor to deck." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed prejob meeting prior to rig up casing running equipment." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 7.0 hours. Operational details: Made up cement stand and racked back in derrick. Rigged up to run 20' casing. Removed drilling bails and elevators, installed casing bails and elevators. Observed that 20' casing tong door had problems opening and closing." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Retrieved CTS and hoses from seabed. Meanwhile: Performed prejob meeting prior to run 20' casing." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed 20' casing bushings and slips." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Picked up shoe joint on deck. Verified float by hosing water through it. Made up shoe joint and float collar joint. Thread locked to connection. Experienced problems with Pipedeck Machine (PDM). Claw did not open. Not able to pick up casing joints from pipedeck to catwalk." "On 2013-04-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 36m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Troubleshoot and repaired Pipedeck Machine (PDM). Found tilt function and boom extension not working. Meanwhile: Performed general maintanence." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 36m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Troubleshoot and repaired PDM (Pipe Deck Machine) Replaced solenoid valve. Meanwhile: Performed general maintenance." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Ran in hole with 20' casing from 36 m MD to 150 m MD. Average running speed 2,2 joints/hour. Filled every joint." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 188m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held pre-job meeting with oncoming crews prior to run 20' casing. Checked all equipment and barriers." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 188m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Picked up and installed casing circulation tool. Tested circulation tool, experienced TDS wash pipe leaking." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 188m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Replaced TDS wash pipe and pressure tested same to 100 bar / 10 minutes. Meanwhile changed leaking hydraulic fittings on elevators." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 201m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran in hole with 20' casing from 188 m MD to 201 m MD." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 201m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cross threaded box joint 105 with pin joint 104, unable to obtain required torque. Decided to lay down both joints. Observed problems with laying down casing joints using HTS." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 201m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Decided to lay down joints manually using deck crane. Performed toolbox talk prior to laying down the joints. Laid out 2 x damaged joint to deck using deck crane." "On 2013-04-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 656m. The activity was categorized as 'drilling -- casing' and lasted for 10.0 hours. Operational details: Ran in hole with 20' casing from 201 m MD to 656 m MD. Average running speed 3-5 joints/hour. Filled every joint with SW. Performed pre-job meeting with oncoming crews prior to run 20'. Checked all equipment and barriers." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1208m. The activity was categorized as 'drilling -- casing' and lasted for 9.0 hours. Operational details: Ran in hole with 20' casing from 656 m MD to 1208 m MD. Average running speed 5 joints/hour. Filled every joint with SW." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1208m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Performed pre-job meeting. Rigged down casing circulation tool. Removed 20' casing elevator and installed 5 1/2' DP elevator." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1208m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up 18 3/4' wellhead with 20' casing pup to string. Not able to obtain correct torque turn graph. Decided to replace wellhead with backup." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1208m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: Broke out wellhead from string and laid down same to deck. Pulled out of hole with 20' casing string from 1208 m to 1195 m and broke out joint with damaged box threads, laid down same to deck. Picked up and made up new 20' casing joint and ran in hole to 1208 meter. Changed to 5 1/2' handling equipment. Prepared backup wellhead on HTS, made up same to running tool. Picked up and made up backup wellhead assembly. Installed plug set in backup wellhead assembly." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1223m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed casing bushings and slips. Ran in hole with 20' casing on landing string from 1208 m to 1223 m. Installed 5 1/2' slips." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1223m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Rigged down 20' casing handling equipment. Moved casing string at regular intervals, no overpull or down weight observed." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1223m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Performed pre-job meeting. Replaced 20 ft bails with drilling bails. Installed BX elevator dressed for 5 1/2' DP." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1327m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Ran in hole with 20' casing on 5 1/2' HWDP landing string from 1223 m MD to 1327 m MD. Rigged up chain hoists in moonppol to center wellhead while running same through deck levels of platform. At 1327 meter sat down 20 Ton. Pulled back to 1317 meter and connected TDS to string." "On 2013-04-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1344m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Established circulation in increments of 300 liter/min. Washed down 20' casing from 1327 m to 1344 m with 1000 liter/min, 30 bar. No excessive weight observed." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1317m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up cement stand. Not able to spin in TDS." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1317m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Troubleshoot TDS spinning problem. Meanwhile: Racked back cement stand. Reciprocated 20' casing string. Made up cement stand into string." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Established circulation in increments of 300 liter/min. Washed down 20' casing from 1344 m to 1358 m with 1000 liter/min, 30 bar. No excessive weight observed. Recorded up / down weights 245 / 183 Ton." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Landed 20' casing at 1358 meter by setting down 15 Ton on hanger. Performed over pull test to 270 Ton. ( 25 Ton overpull)" "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Started production on F-12. Circulated 250 m3 with 2300 liter/min, 40 bar. Lined up, flushed and pressure tested surface lines to 345 bar for 10 min." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- other' and lasted for 6.0 hours. Operational details: Dropped ball for bottom wiper plug. Applied 20 bar against lo-torq valve, opened same to verify lineup. Mixed and pumped 308 m3 of 1,56 SG lead cement slurry with 1000-1050 l/min, 22-19 bar. Mixed and pumped 30 m3 of 1,92 SG tail cement slurry with 840 l/min, 17 bar. Released top dart and reset stroke counters." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Displaced 3000 liter SW from cement unit using cement pump. Did not observe top plug shear after +/- 820 liters as prognosed. Continued to displace with SW using rig pumps at 3900 liter/min, 45-50 bar. After 2990 liter pumped observed pressure spike of 111 bar. Indicating top plug sheared. Under displaced with 10 m3, did not bump plug. Total displacement 201 m3 SW. Bleed back pressure to trip tank and monitored for backflow, no flow observed. Disconnected cement hose and removed same." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Released 18 3/4' CART tool from hanger. Performed pre-job meeting prior to laying out cement head and CART." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Laid down cement head with 5 1/2' HWDP single down on HTS. Connected TDS and circulated 2 ea. sponge balls through pipe. POOH with 18 3/4' CART on 5 1/2' HWDP from 140 meter to surface. Laid down 18 3/4' CART to cantilever." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Held tool box talk with ROV and deck crew. Assisted ROV and deck crew with installing riser guide funnel. Meanwhile: Dismantled TDS washpipe. Cleaned and cleared rigfloor and prepared to spot equipment for HPDR running. Installed teflon riser guides in hole openings on centralizer and tension decks." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to pickup and prepare HPDR equipment." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up Claxton tool and torqued up handling pup connection, laid down same to cantilever. Meanwhile: Spotted riser equipment on cantilever, centralizer and tension decks." "On 2013-04-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Installed tension ring on centralizer deck. Meanwhile: Organized riser joints on cantilever. Connected BOP joint to Claxton tool." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: Rigged up and prepared to run HPDR. Picked up HPU unit and tested Claxton running tool on cantilever. Connected Claxton tool to top riser joint, pressure tested same to 35 bar, OK. Performed pre-job meeting with oncoming crews." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed master bushings and installed riser spider. Function tested riser spider and removed lifting bridal." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed pre-job meeting prior to run HPDR." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up TBC / Stress joint and ran through rotary, landed same in spider." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up lower riser pup joint. Prepared seal faces on joint connection and landed same onto TBC / Stress joint in rotary." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- wait' and lasted for 5.5 hours. Operational details: Not able to make up flange between riser joints due to studs too long. Technical Team fabricated spacer washer for shimming hydraulic jacks. Meanwhile: Rigged up wires for guide line system in moonpool. Prepared next riser joints on cantilever deck." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Made up connection between TBC / Stress joint and lower riser pup joint. Installed fairings (Anti collision protection). Meanwhile: Installed lift nubbin on riser joint #4." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Function tested TBC in moonpool, functions OK. Observed minor leak from hotstab dummy with valves on TBC valve panel in open position. Checked position of valves and confirmed with town. Shut valves on TBC valve panel. No leak observed." "On 2013-04-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ran in hole from 12 m to 21 m with HPDR. Picked up joint #4, removed lift nubbin and checked seal faces." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Made up connection between lower riser pup joint and joint #4. Installed fairings (Anti collision protection). Meanwhile: Installed lifting nubbin on joint #3." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Ran in hole with riser. Connected guide line wires to guide ring on stress joint. Continued to RIH with riser from 21 m to 35 m." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up joint #3, removed lift nubbin and checked seal faces. Made up connection between riser joints #3 and #4 and tested same. Installed fairings (Anti collision protection). RIH with riser from 35 m to 50 m." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW due to significant sea above 2 meter. Meanwhile: Worked with installation of TDS washpipe. Prepared HPDR joints on cantilever." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up joint #6, removed lift nubbin and checked seal faces. Made up connection between riser joints #6 and #3 and tested same. Not able to obtain pressure test." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Broke out connection between riser joints #6 and #3 and inspected same. Found o-ring missing. Installed o-ring in outer groove. Made up connection between riser joints #6 and #3 and re-tested same to 35 bar, test ok." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 65m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Installed fairings (Anti collision protection). RIH with HP drilling riser through splash zone from 50 m to 65 m." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 65m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up joint #7, removed lift nubbin and checked seal faces. Made up connection between riser joints #7 and #6 and tested same. Not able to obtain pressure test." "On 2013-04-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 65m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: Broke out connection between riser joints #6 and #7 and inspected same. Replaced o-ring." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 65m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Made up connection between riser joints #6 and #7 and re-tested same to 35 bar, test ok." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: RIH with HP Drilling Riser from 65 m to 103 m." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged up handling equipment prior to pick up tension joint. C-plate, long bails and elevators." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.0 hours. Operational details: Held pre-job meeting prior to make up tension joint. Picked up tension joint, removed lift nubbin and checked seal faces, polished light scratches on tension joint sealface. Made up connection between riser joints and tested same. Installed fairings (Anti collision protection). RIH with HPDR from 103 m to 121 m. Meanwhile: Installed second guide wire on WHH." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged up handling equipment prior to pick up BOP joint, drilling bails and BX elevators." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up BOP joint, removed lift nubbin and checked seal faces. Made up connection between BOP and tension joints, tested same. Meanwhile: Prepared landing joint with side entry sub. Prepared equipment for installation of tension ring." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Removed c-plate. Prepared to run Claxton tool and BOP joint through rotary. Removed riser spider." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 127m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran in with HPDR from 121 m to 127 m. Installed master bushing." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 127m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held pre-job meeting prior to land riser. Picked up and made up landing string to TDS. Came down to land riser. Due to sideways movement the riser hit top of guide funnel. The funnel fell off the WHH." "On 2013-04-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 127m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Performed pre-job meeting. Recovered riser guide funnel to surface for inspection and repair." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 127m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Recovered riser guide funnel to surface for inspection and repair. Meanwhile: Worked with installation of new washpipe." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 127m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Repaired broken spindle on riser guide funnel. Meanwhile: Worked with installation of new washpipe." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 127m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: Launched and installed riser guide funnel on WHH." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Held pre-job meeting prior to land riser. Came down with riser and stabilized TBC around WHH. Released riser guide funnel from WHH. Oriented TBC and landed same with 22 ton down weight." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: ROV installed hot stab into TBC and operated valves to lock position. Pressured up mini reel 3000 psi / 15 min to lock TBC. ROV operated valves into park position." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Performed overpull test on riser to 15 Ton. Replaced hot stab with dummy hot stab." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held pre-job meeting prior to pressure test riser and 20' casing. Rigged up cement hose and lo-torq valve on drill floor. Attempted to pressure test lines and hose to 150 bar. Not able to obtain line test." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Troubleshot leak in surface lines. Replaced lo-torq valve. Pressure tested lines and hose to 150 bar / 10 min." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Filled riser with SW and evacuated air from system. Lined up and performed pressure test of riser and 20' casing to 100 bar / 10 min." "On 2013-04-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Held pre-job meeting prior to rig up tensioner system. Worked with installation of centralizer and boat collision stool. Meanwhile: Installed new washpipe." "On 2013-04-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Installed centralizer and boat collision stool. Meanwhile: Installed new washpipe." "On 2013-04-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: Installed tensioner ring and cylinders. Meanwhile: Replaced soloniod valve on TDS spin function." "On 2013-04-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Performed pre-job meeting. Load shifted from TDS to tension cylinders. Final tension on cylinders adjusted to 150 Ton." "On 2013-04-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Released Claxton tool and pulled back same to drill floor. Broke out and laid down Claxton tool to deck." "On 2013-04-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Prepared for skidding BOP to wellcenter. Rigged up scaffolding for accessing NT2 connector. Held toolbox talk prior to skidding and landing BOP. Skidded BOP to wellcenter and landed same. At 1600 hrs. started production on well F-12 and F-14." "On 2013-04-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 8.0 hours. Operational details: Nippled up BOP, slip joint and diverter systems." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Nippled up BOP, slip joint and diverter systems." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: RIH with BOP test plug on 5 1/2 DP. Tested BOP and HPDR connections to 30 bar / 5 min - 345 bar / 10 min. POOH with BOP test plug." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Made up seat protector and RIH. Installed seat protector and POOH with RT." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Installed new type wash pipe." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Continued to install new wash pipe. Tested same to 275 bar." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 232m. The activity was categorized as 'drilling -- trip' and lasted for 7.5 hours. Operational details: Picked up and made up 17 1/2' drilling BHA and RIH on 5 1/2' HWDP from surface to 232 meter." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 232m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Held toolbox talk. Performed choke drills with both crews." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 473m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Picked up 5 1/2' DP singles while RIH with 17 1/2' BHA from 232 m to 473 m. Average tripping speed 120 m/hr." "On 2013-04-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1159m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 473 m to 1159 m. Average tripping speed 343 m/hr." "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1236m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 1159 m to 1236 m. Average tripping speed 154 m/hr. Observed 5 Ton loss in weight at 1236 meter. Recorded up / down weights 133 / 115 Ton." "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1262m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Washed / reamed down from 1236 m to 1262 m with 1500 l/min, 19 bar, 20 RPM, 4-8 kNm. At 1262 meter tagged firm cement with 5 Ton" "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1265m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled firm cement from 1262 m to 1264,8 m with 3560 l/min, 105 bar, 40 RPM, 6-15 kNm, WOB 4-5 Ton. Performed pre-job meeting prior to displacement job. Observed leak on longitudinal flowline on main deck." "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1265m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Stopped drilling and repaired leak." "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1266m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled top plug from 1264,8 m to 1265,6 m with 3500 l/min, 106 bar, 40 RPM, 6-19 kNm, WOB 4-5 Ton. Observed black rubber pieces coming across shakers." "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1266m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: Displaced well from SW to 1,40 sg OBM with 3530 l/min, 150 bar. Diverted SW returns to sea." "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1266m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: Circulated and conditioned OBM while reciprocating string from 1240 m to 1255 m with 20 rpm, 2-6 kNm. Increased pump rate in incremens of 110 l/min to ensure shakers and surface system do not over flow." "On 2013-04-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1356m. The activity was categorized as 'drilling -- drill' and lasted for 13.0 hours. Operational details: Drilled firm cement from 1265,6 m to 1356 m with 3000-3520 l/min, 183 bar, 40-90 RPM, 2-10 kNm, WOB 5-10 Ton. Drilled bottom wiper plug at 1358 m to 1358,7 m. Observed black / red rubber pieces coming across shakers." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1365m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled firm cement from 1365 m to 1368 m with 3700 l/min, 190 bar, 60-90 RPM, 5-20 kNm, WOB 3-10 Ton. Cleaned out rathole 3 times." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled new formation from 1365 m to 1368 m with 3700 l/min, 188 bar, 90 RPM, 2-8 kNm, WOB 5-10 Ton." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Pulled bit inside shoe. Circulated until even MW in out 1,40 sg with 3700 liter/min, 180 bar, 20 rpm, 5 kNm." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1368m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 3.5 hours. Operational details: Performed pre-job meeting prior to FIT. Confirmed line up down string through TDS. Attempted to pressure test surface lines against upper / lower IBOP. No test obtained. Disconnected TDS and installed pump in sub. Attempted to pressure test surface lines against pump in sub. No test obtained." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1368m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 4.5 hours. Operational details: Performed internal test of cement unit. Not able to obtain good test. Investigated problems on unit. By-passed shutt-off valve. Obatined good pressure test on cement unit. Meanwhile: Circulated and pumped with 3500 liter/min, 173 bar, 60 rpm, 7-9 kNm. Performed pre-job meeting prior to FIT." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1368m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Lined up to pump down string through TDS Pressure tested lines to 30 / 200 bar - 5 /10 minutes. Spaced out and closed upper pipe ram. Performed FIT to 1,55 sg EMW using 1,40 sg mud. Pumped 320 liter from 5 bar to 20 bar at cement unit with 40 liter/min. Bled back 320 liter." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Washed and reamed rathole with 4420 l/min, 256 bar, 60 RPM, 5-6 kNm" "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 17 1/2' hole from 1368 m to 1400 m with 3675-4455 l/min, 188-257 bar, 60-140 RPM, 7-15 kNm, WOB 5 Ton, ECD 1,446-1,449 sg. 5 ea. cuttings screw conveyors plugged up." "On 2013-04-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- other' and lasted for 9.0 hours. Operational details: Worked with unplugging cuttings screw conveyors. Meanwhile: Monitored well on trip tank and worked string from 1324 m to 1360 m." "On 2013-04-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Worked with unplugging cuttings screw conveyors. Established circulation with 4500 liter/min, 280 bar. Shakers and cuttings screw conveyors handled returns as required. Meanwhile: Monitored well on trip tank and worked string from 1324 m to 1360 m. Up / down weights 130 / 115 Ton." "On 2013-04-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Washed down from 1360 m to 1400 m with 4400 liter/min, 274 bar, 60 rpm, 8 kNm. Performed survey. Rupture disk tripped on MP #1 and MP #2. Replaced rupture discs." "On 2013-04-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- drill' and lasted for 10.5 hours. Operational details: Drilled 17 1/2' hole from 1400 m to 1500 m with 3990-4300 l/min, 165-246 bar, 100-140 RPM, 7-11 kNm, WOB 1-3 Ton, ECD 1,434-1,448 sg." "On 2013-04-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.0 hours. Operational details: Waited on weather. Not able to back load cuttings from ISO tanks to supply vessel due to heavy wind and sea. Meanwhile: Circulated hole clean at 1500 meter with 4300 liter/min, 248 bar. Pulled back into shoe. Circulated with 1440 liter/min, 35 bar. Picked up and racked back 5 1/2' DP." "On 2013-04-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 16.0 hours. Operational details: Waited on weather. Not able to back load cuttings from ISO tanks to supply vessel due to heavy wind and sea. Meanwhile: Circulated with 1440 liter/min, 35 bar. Picked up and racked back 5 1/2' DP, 23 stands racked back." "On 2013-04-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- other' and lasted for 7.0 hours. Operational details: Back loaded cuttings from ISO tanks to supply vessel, Total 40 Ton." "On 2013-04-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 1333 m to 1482 m. Average tripping speed 298 m/hr. Continue to back load cuttings from ISO tanks to supply vessel." "On 2013-04-15, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Washed and reamed down from 1482 m to 1493 m with 3200 liter/min, 168 bar, 30 rpm, 9 kNm. Lost all rig power supply on the rig due to work on faulty gas detector." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Restarted all rig systems. Meanwhile: Lined up and observed well on trip tank. Rotated string periodically to ensure free movement." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Restarted all rig systems. Meanwhile: Established circulation with 440 liter/min, 7 bar. Reciprocated pipe." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1500m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Continue to back load cuttings from ISO tanks to supply vessel." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1573m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 17 1/2' hole from 1500 m to 1573 m with 4275-4320 l/min, 257-265 bar, 120-140 RPM, 9-11 kNm, WOB 5-8 Ton, ECD 1,441-1,449 sg. Average ROP 16,2 meter/hour. Drilled with reduced drilling rate due to surface cuttings transfer system restriction." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1685m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 17 1/2' hole from 1573 m to 1685 m with 4320 l/min, 254-260 bar, 140 RPM, 10-15 kNm, WOB 5-6 Ton, ECD 1,431-1,442 sg, max gas 0,57 %. Average ROP 22,5 meter/hour. Drilled with reduced drilling rate due to surface cuttings transfer system restrictions." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' hole from 1685 m to 1780 m with 4320 l/min, 256-262 bar, 140 RPM, 12-15 kNm, WOB 5-6 Ton, ECD 1,438-1,443 sg, max gas 0,46 %. Average ROP 15,8 meter/hour. Drilled with reduced drilling rate due to surface cuttings transfer system restrictions. Stopped drilling due to full ISO tanks. Not able to back load cuttings from ISO tanks to supply vessel due to heavy wind and sea." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: Circulated hole clean 4300 liter/min, 254 bar, 120 rpm, 7 kNm." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 17 1/2 BHA on 5 1/2' DP from 1765 m to 1346 m. Average tripping speed 838 m/hr." "On 2013-04-16, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waited on weather. Not able to back load cuttings from ISO tanks to supply vessel due to heavy wind and sea. Meanwhile: Circulated with 1420 liter/min, 65 bar." "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather. Not able to back load cuttings from ISO tanks to supply vessel due to heavy wind and sea. Meanwhile: Circulated with 1420 liter/min, 65 bar." "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.0 hours. Operational details: Waited on weather. Meanwhile service TDS and PRS`s. Change valves on MP # 3" "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Backload cuttings to boat. Meanwhile circ with 1410lpm" "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Unable to start screw conveyor. Continue circ." "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Test run augers. Meanwhile circ with 1420lpm" "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: TBT. RIH from 1345-1765m." "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1780m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Wash in from 1765-1780m with 3300lpm, 30 RPM, 7Nm TRQ. Take SCR at 1780m." "On 2013-04-17, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1812m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Drilled from 1780-1812m" "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1944m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and orientated 17 1/2' hole from 1812 m to 1944 m with 4300 lpm, 270 bar, ECD 1.44 sg, WOB 5-7 MT, 140 rpm, 13-15 kNm, Inst. ROP 40 m/hr, Average ROP 26 m/hr." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1963m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled and orientated 17 1/2' hole from 1944 m to 1963 m at reduced ROP due to cuttings handling system with 4000 lpm, 240 bar, ECD 1.44 sg, WOB 4 MT, 140 rpm, 12-13 kNm, Inst. ROP 30 m/hr, Average ROP 19 m/hr. Last survey: 1950.9m MD, 15.46 incl, 264.1 azimuth" "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1966m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled and orientated 17 1/2' hole from 1963 m to 1966 m with 4000 lpm, 240 bar, ECD 1.44 sg, WOB 4 MT, 140 rpm, 12-13 kNm, Inst. ROP 30 m/hr. Unable to back load cuttings from ISO pumps to supply vessel due to high wind and sea state. Commenced circulating hole clean." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1966m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather to back load cuttings. Circulated hole clean while reciprocating and rotating string with 4300 lpm, 267 bar, 120 rpm, 9 kNm, ECD 1.43 sg." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1898m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: Waited on weather to back load cuttings. Racked back 5 1/2' DP stand. Circulated hole clean while reciprocating and rotating string with 4300 lpm, 267 bar, 120 rpm, 9 kNm, ECD 1.42 sg." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1898m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to back load cuttings. Held TBT and flowchecked well for 15 min - well static." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather to back load cuttings. POOH with 5 1/2' DP wet from 1898 m to 1320 m inside 20' shoe." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1320m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: Waited on weather to back load cuttings. Flow checked well for 15 min - well static" "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1318m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.5 hours. Operational details: Waited on weather to back load cuttings. Meanwhile: Circulated with 1400 lpm, 30 bar, 0 rpm." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1318m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Called in supply vessel and hook up ISO pumps overboard hose. Meanwhile: Circulated with 1400 lpm, 30 bar, 0 rpm. Function tested BOP" "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1308m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Back loaded cuttings from ISO pump # 1 to supply vessel. Meanwhile: Pulled back 10 m and circulated with 1400 lpm, 30 bar, 0 rpm." "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1308m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Back loaded cuttings from ISO pump # 2 to supply vessel. Cuttings transfer line plugged-up after 15 m3 pumped. Cleared lines and stood off supply vessel due to heavy wind and sea. Meanwhile: Circulated with 1400 lpm, 30 bar, 0 rpm. Held PDSA meeting with all available personale" "On 2013-04-18, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1308m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on weather to back load cuttings. Meanwhile: Circulated with 1420 lpm, 33 bar, 0 rpm. Held PDSA meeting with all available personale" "On 2013-04-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1308m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 15.5 hours. Operational details: Waited on weather to back load cuttings. Meanwhile: Circulated with 1420 lpm, 33 bar, 0 rpm." "On 2013-04-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1308m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Called in supply vessel and back loaded cuttings from ISO pumps." "On 2013-04-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1950m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Held TBT. RIH on 5 1/2' DP from 1308 m to 1950 m. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1365m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Washed down from 1950 m to 1965 m with 3300 lpm, 183 bar, 40 rpm, 8 kNm. Recorded SCRs at 1965 m. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1984m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Established drilling parameters. Drilled and orientated 17 1/2' hole from 1966 m to 1984 m at reduced ROP to establish rig solids control system running with cuttings prior to swiching to ISO pump system. Drilling parameters: 4300 lpm, 275 bar, 120 rpm, 10-12 kNm, WOB 5-6 MT, Inst ROP 15 m/hr, ECD 1.44 SG. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-19, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2046m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled and orientated 17 1/2' hole from 1984 m to 2046 m with 4300 lpm, 275 bar, 140 rpm, 12-15 kNm, WOB 8-10 MT, Inst ROP 35 m/hr, ECD 1.44 SG. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2113m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and orientated 17 1/2' hole from 2046 m to 2113 m with 4300 lpm, 285 bar, 140 rpm, 13-15 kNm, WOB 9-11 MT, Inst ROP 35 m/hr, ECD 1.44 SG. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2178m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and orientated 17 1/2' hole from 2113 m to 2178 m with 4230 lpm, 283 bar, 140 rpm, 12-16 kNm, WOB 8-10 MT, Inst ROP 35 m/hr, ECD 1.43 SG. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2290m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled and orientated 17 1/2' hole from 2178 m to 2290 m with 4252 lpm, 282 bar, 140 rpm, 16-19 kNm, WOB 12-16 MT, Inst ROP 35 m/hr, ECD 1.43 SG. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2330m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled and orientated 17 1/2' hole from 2290 m to 2330 m with 4230 lpm, 282 bar, 140 rpm, 16-19 kNm, WOB 9-11 MT, Inst ROP 10 m/hr, ECD 1.42 SG. Meanwhile: Back loaded cuttings to supply vessel Flushed U-tube with fresh mud" "On 2013-04-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2378m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and orientated 17 1/2' hole from 2330 m to 2378 m with 4250 lpm, 283 bar, 140 rpm, 15-17 kNm, WOB 9-12 MT, Inst ROP 25 m/hr, ECD 1.43 SG. Identified Balder formation at 2373 m. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-20, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2475m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and orientated 17 1/2' hole from 2378 m to 2475 m with 4300 lpm, 287 bar, 140 rpm, 20-25 kNm, WOB 18-20 MT, Inst ROP 25 m/hr, ECD 1.43 SG. Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2540m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and orientated 17 1/2' hole from 2475 m to 2540 m with 4300 lpm, 292 bar, 140 rpm, 20-25 kNm, WOB 18-20 MT, Inst ROP 35 m/hr, ECD 1.44 SG. Identified Lista formation at 2512 m Meanwhile: Back loaded cuttings to supply vessel" "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled hole clean from 2540 m to 2570 with 4250 lpm, 290 bar, 140 rpm, 15-20 kNm, WOB 7-10 MT, Inst ROP 10 m/hr, ECD 1.43 SG." "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2574m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled hole clean from 2570 to 17 1/2' section TD at 2574 m with 4250 lpm, 290 bar, 140 rpm, 15-20 kNm, WOB 7-10 MT, Inst ROP 10 m/hr, ECD 1.43 SG. Final TD called at 07:20 hrs." "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2464m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.5 hours. Operational details: Circulated hole clean with 4286 lpm, 289 bar, 140 rpm, 11-15 kNm, ECD 1.42 SG. Circulated total 3 B/U racking one 5 1/2' DP stand on every B/U while increasing mud weigth 2 points to 1.42 sg. Meanwhile: Back loaded cuttings to supply vessel and stood off same. 4 empty ISO pumps onboard." "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2169m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Flow checked well for 15 min - well static. POOH 17 1/2' BHA on 5 1/2' DP 10 stands wet from 2464 m to 1354 m." "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1354m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Pumped slug and POOH 17 1/2' BHA on 5 1/2' DP from 2169 m to 1354 m. No overpull observed." "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 272m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH 17 1/2' BHA on 5 1/2' DP/HWDP from 1354 m to 272 m. Flow checked for 15 min - Well Static." "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: Held TBT. POOH 17 1/2' BHA from 272 m to surface. Racked back 2 x 8 1/4' DC stands and layed out remaining 17 1/2' BHA. Bit grading: 1.3.WT.G.X.I.BT.TD" "On 2013-04-21, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Cleaned and cleared drill floor. Isolated drilling equipment, inspected and serviced same" "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Serviced and inspected drilling equipment and deisolated same." "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 142m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up seat protector retrival tool and jet sub. RIH seat protector retrival tool to 137 m. Washed down from 137 m to 142 m with 2860 lpm, 54 bar. Engaged seat protector with 3 MT and 0.5 left hand turn." "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with seat protector and dressed well head with 2770 lpm, 51 bar. Layed out seat protector and running tool." "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held TBT. R/U casing handling equipment" "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: R/U casing handling equipment." "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Held TBT. P/U 14' float shoe and installed bypass baffle. P/U and M/U Intermmediate and landing collar 14' casing joints. Tested float and RIH shoetrack to 33 m." "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 327m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH 14' 169.65 kg/m csg from 33 m to 327 m filling every joint with 1.42 sg OBM. Average running speed 6 jts./hr." "On 2013-04-22, at Well NO 15/9-F-11, a drilling event occurred at a depth of 854m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH 14' 169.65 kg/m csg from 327 m to 854 m filling every joint with 1.42 sg OBM. Average running speed 8 jts./hr." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 901m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH 14' 169.65 kg/m csg from 854 m to 901 m filling every joint with 1.42 sg OBM. Lowered TDS to 3 m above rig floor, tilted bails forward to pick up 14' 169.65 kg/m casing joint. When tilting forward a bolt on one out of four U-clamps sheared off. No personale in the area. Potential 0.12kg*4m*9.81=5J." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 901m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Isolated drilling equipment replaced broken U-clamp and inspected remaining three U-clamps. No wear or damage observed." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 935m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH 14' 169.65 kg/m csg from 901 m to 953 m filling every joint with 1.42 sg OBM. Average running speed 6 jts./hr. Observed link arms pushing against U-clamp bolts on bails when using link tilt drill function." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 935m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Isolated drilling equipment and inspected same. Evaluated situation and formulized plan forward to only use link tilt retract function, thereby eliminating the pushing action on the bails." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1057m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH 14' 169.65 kg/m csg from 935 m to 1057 m filling every joint with 1.42 sg OBM. Average running speed 6 jts./hr." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1247m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH 14' 169.65 kg/m csg from 1057 m to 1247 m filling every joint with 1.42 sg OBM. Average running speed 6 jts./hr. Observed leaking hose power tong." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1247m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Changed out leaking hydraulic hose and connections on power tong." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH 14' 169.65 kg/m csg from 1247 m to 1348 m filling every joint with 1.42 sg OBM. Average running speed 6 jts./hr. Engaged fill up and circulation tool [FAC]. Broke circulation with 200 lpm, 10 bar. Staged up pumps in 100 lpm incriments to 1000 lpm, 14,7 bar. Dis-engaged FAC. Observed connection on pack-off backed out." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1348m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Made up connection on pack-off. Checked and re-tightent allen screw lock keys securing pack-off on FAC." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1527m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH 14' 169.65 kg/m csg from 1348 m to 1527 m filling every joint with 1.42 sg OBM. Average running speed 7 jts./hr. Unable to function power tong stabbing guide due to broken fitting on hydraulic hose." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1527m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Removed hydraulic hose on stabbing guide and blanked off fitting on power tong." "On 2013-04-23, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2133m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: RIH 14' 169.65 kg/m csg from 1527 m to 2133 m filling every joint with 1.42 sg OBM. Average running speed 8 jts./hr." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2424m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH 14' 169.65 kg/m csg from 2133 m to 2424 m filling every joint with 1.42 sg OBM.Recorded Up/Dw weight 430/320 MT. Average running speed 8 jts./hr." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2424m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2424m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U and M/U 14' casing hanger. Attempted to pick up 14' casing hanger and RIH. Observed draw work drum pay out." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2433m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Troubleshoot drawwork failure. Meanwhile: Removed auto slips and lowered 14' casing hanger below rotary in a controlled sequence, Up/Dw weight 430/320 MT. Installed master bushing and made up circulation swedge. Circulated with 200 lpm, 9 bar, 14' casing shoe at 2433 m." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2433m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Shot down pumps and flowchecked. R/D casing power tong, circulation swedge and surface lines." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2552m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH 14' 169.65 kg/m casing on 5 1/2' HWDP from 2433 m to 2516 m. Washed down from 2516 m to 2552 m with 500 lpm, 11 bar" "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2552m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Recorded hole restriction at 2552 m. Worked and washed pass restriction with 1000 lpm, 16 bar, Up/Dw weight 440/318 MT." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2571m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: M/U cement assembly and landed hanger at HOP 140.38 m. Set down 7 MT and marked pipe. Picked up and recorded 45 MT overpull, marked pipe. Rotated landing string one right hand turn and verified stem free." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: R/U cement hoses and circulated 1.5 B/U with 3000 lpm, 60 bar. No losses observed." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Pumped 25 m3 of 1.75 SG spacer and dropped bottom dart. Mixed and pumped 24 m3 of 1.90 SG cement slurry, 600 lpm. Displaced the cement to the rig floor with 0.88 m3 and dropped top dart. Zeroed stroke counters and displaced cement with 183 m3, 8262 strokes of 1.42 SG mud, 2970 lpm. Observed bottom plug shear after 7290 strokes." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Stepped down pumps to 500 lpm, FCP 31 bar and bumped top plug after 188 m3, 8480 strokes pumped. Pressured up t0 90 bar/10 min and eqaulized lines to cement unit." "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Pressure tested casing to 340 bar/10 min, 2.2/2.2 m3 Pumped/Returned" "On 2013-04-24, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Slacked off weight and marked pipe. Picked up 45 MT overpull test, slacked of and rotated pipe 3.5 RH turns, Marked pipe and recorded 8.5' travel. Sat seal assembly with 207 bar/10 min and picked up 45 MT." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Closed annular preventer and attempted to pressure test seal assembly to 345 bar/10 min - NoGo. Unable to establish decreasing trend." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Released hanger running tool. L/O cement head and circulated wash balls. POOH and L/O hanger running tool." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: M/U wearbushing running and combination tool. RIH and set wear bushing." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: Tested seal assembly and lower pipe rams to 345 bar/15 min." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.5 hours. Operational details: Tested BOPs and surface lines 20/345 bar, 5/10 min." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed wear bushing. POOH wear bushing running tool and L/O same" "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ceaned and cleared rig floor. Serviced drilling equipment prior to tripping." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 176m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Held TBT. P/U and M/U 12 1/4' Drill out BHA. RIH on 5 1/2' HWDP to 176 m." "On 2013-04-25, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1625m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: RIH 12 1/4' drill out BHA on 5 1/2' DP from 176 m to 1625 m filling every 1000 m with 1.42 sg OBM. Performed choke drill with both crews." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2477m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: RIH 12 1/4' drill out BHA on 5 1/2' DP from 1625 m to 2477 m filling every 1000 m with 1.42 sg OBM." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2541m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Washed down from 2477 m to 2541 m with 1500 lpm, 50 bar, 30 rpm, 7-10 kNm, recorded Up/Dw weight 159/133 MT. Tagged TOC at 2541 m with 5 MT." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled shoetrack and shoe from 2541 m to 2571 m with 2500 lpm, 117 bar, 40/80 rpm, 12-15 kNm, WOB 8-16 MT Reduced MW from 1.42 sg to 1.28 sg" "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2577m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Cleaned out rat hole and drilled 3 m new formation from 2571 m to 2577 m with 2500 lpm, 95 bar, 80 rpm, 17-22 kNm, WOB 10 MT" "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2557m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Pulled back from 2577 m to 2557 m inside 14' casing. Circulated even MW In/Out 1.28 sg." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2557m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: Lined up cement unit and pressure tested lines. Performed FIT to 1.65 sg EMW, 91 bar surface pressure." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Dropped gyro survey tool. Pumped 2 m3 slug and chased same with 1500 lpm, 30 bar. Landed out gyro tool and recorded survey." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH to 2517 m while recording gyro survey. Reduced tripping speed due to gyro survey while POOH. Meanwhile: Held TBT for encoder change out." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2517m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Attempted to change out Top drive encoder." "On 2013-04-26, at Well NO 15/9-F-11, a drilling event occurred at a depth of 216m. The activity was categorized as 'drilling -- trip' and lasted for 7.0 hours. Operational details: POOH on 5 1/2' DP from 2517 m 216 m while recording gyro survey. Reduced tripping speed due to gyro survey while POOH. Flow checked well for 10 min - well static." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: L/D and racked back 12 1/4' Drill Out BHA and 5 1/2' HWDP." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 46m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Held TBT. P/U and M/U 8 1/2' steerable BHA to 46 m." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled back and plugged in tools. Observed problem with SoundTrack tool." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 7m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: Troubleshoot SoundTrack tool. POOH to 7 m and plugged into OnTrack tool, verified software communication." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 205m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: P/U and M/U 8 1/2' steerable BHA including 5 1/2' HWDP to 205 m" "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1010m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RIH 8 1/2' steerable BHA on 5 1/2' DP from 205 m to 1010 m." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1010m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Filled string with 1.28 sg OBM and shallow tested MWD tools." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1537m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH 8 1/2' steerable BHA on 5 1/2' DP from 1010 m to 1537 m, filled string every 1000 m." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2142m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: RIH 8 1/2' steerable BHA on 5 1/2' DP singles from 1537 m to 2142 m, filled string every 1000 m." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2142m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Removed auto slips and installed master bushing." "On 2013-04-27, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2142m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Held TBT. Slipped and cut drill line." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2142m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: Slipped and cut 44 m drill line." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2142m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Calibrated block hight and cleaned and cleared rig floor." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2142m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Removed master bushing and installed auto slips." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2142m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH 8 1/2' steerable BHA on 5 1/2' DP from 2142 m to 2546 m." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2577m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Broke circulation and recorded SCRs. Washed down and tagged bottom at 2577 m with 1800 lpm, 112 bar, 0 rpm - No fill or junk in hole." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2629m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Established drilling parameters. Drilled and orientated 8 1/2' hole from 2577 m to 2629 m with 1800 lpm, 120 bar, 60 rpm, 12-15 kNm, WOB 8 MT, Gross ROP 20 m/hr, Net ROP 13 m/hr, ECD 1.34 SG Registred de-coding problem with MWD tools." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2629m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Troubleshoot de-coding problem with MWD tools." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2826m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 2629 m to 2826 m with 2200 lpm, 172 bar, 140 rpm, 15-18 kNm, WOB 8 MT, Gross ROP 40 m/hr, Net ROP 28 m/hr, ECD 1.36 SG Top Shetland at 2822 m." "On 2013-04-28, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2907m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 2826 m to 2907 m with 2200 lpm, 172 bar, 180 rpm, 15-20 kNm, WOB 6-8 MT, Gross ROP 30 m/hr, Net ROP 20 m/hr, ECD 1.36 SG" "On 2013-04-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2962m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 2907 m to 2962 m with 2200 lpm, 172 bar, 140-180 rpm, 15-20 kNm, WOB 4-9 MT, Gross ROP 30 m/hr, Net ROP 16 m/hr, ECD 1.37 SG. Unable to build required angle." "On 2013-04-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2986m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Reduced ROP to build inclination - good response. Drilled and orientated 8 1/2' hole from 2962 m to 2986 m with 2000 lpm, 144 bar, 180 rpm, 14-16 kNm, WOB 4-5 MT, Gross ROP 15 m/hr, Net ROP 10 m/hr, ECD 1.36 SG. Stepped up ROP in 2.5 m/hr increments to 15 m/hr" "On 2013-04-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 2986 m to 3070 m with 2200 lpm, 175 bar, 180 rpm, 16-20 kNm, WOB 5-10 MT, Gross ROP 30 m/hr, Net ROP 14 m/hr, ECD 1.36 SG. Observed stick slip at WOB above 10 MT" "On 2013-04-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3108m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3070 m to 3108 m with 2200 lpm, 175 bar, 180 rpm, 17-22 kNm, WOB 7-9 MT, Gross ROP 25 m/hr, Net ROP 19 m/hr, ECD 1.36 SG." "On 2013-04-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3108m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Tared CoPilot MWD tool." "On 2013-04-29, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3279m. The activity was categorized as 'drilling -- drill' and lasted for 9.8 hours. Operational details: Drilled and orientated 8 1/2' hole from 3108 m to 3279 m with 2200 lpm, 175 bar, 180 rpm, 17-21 kNm, WOB 7-9 MT, Gross ROP 25 m/hr, Net ROP 18 m/hr, ECD 1.37 SG." "On 2013-04-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3350m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 3279 m to 3350 m with 2200 lpm, 175 bar, 180 rpm, 15-22 kNm, WOB 7-9 MT, Gross ROP 20 m/hr, Net ROP 17 m/hr, ECD 1.38 SG Logging unit shut down" "On 2013-04-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3350m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Picked up off bottom and reciprocated string with 1800 lpm, 160 bar, 60/120 Up//Dw rpm. Purged mud logging unit, re-booted computers, reset and calibrated settings." "On 2013-04-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3443m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3350 m to 3443 m with 2200 lpm, 180 bar, 180 rpm, 15-25 kNm, WOB 8-10 MT, Gross ROP 20 m/hr, Net ROP 12 m/hr, ECD 1.38 SG" "On 2013-04-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3443m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Deleted corupted fill and re-booted computers in mud logging unit." "On 2013-04-30, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3514m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: Drilled and orientated 8 1/2' hole from 3443 m to 3514 m with 2200 lpm, 180 bar, 180 rpm, 15-21 kNm, WOB 7-9 MT, Gross ROP 20 m/hr, Net ROP 11 m/hr, ECD 1.38 SG" "On 2013-05-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3576m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3514 m to 3576 m with 2200 lpm, 185 bar, 180 rpm, 18-22 kNm, WOB 3-5 MT, ECD 1.37 sg. Average ROP: 10 m/hr." "On 2013-05-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3673m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 3576 m to 3673 m with 2500 lpm, 227-230 bar, 180 rpm, 15-24 kNm, WOB 7-10 MT, ECD 1.37-1.40 sg. Average ROP: 17.6 m/hr" "On 2013-05-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3714m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 3673 m to 3714 m with 2500 lpm, 225-228 bar, 180 rpm, 18-20 kNm, WOB 4-6 MT, ECD 1.37-1.40 sg. Average ROP: 11.7 m/hr Drilled with controlled ROP due to lack of surface space for cuttings. Backloaded cuttings at 15:00." "On 2013-05-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3754m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled and orientated 8 1/2' hole from 3714 m to 3754 m with 2000-2500 lpm, 153-228 bar, 180 rpm, 17-26 kNm, WOB 7-10 MT, ECD 1.39-1.40 sg. Average ROP: 14.5 m/hr Reamed one double due to erratic torque readings and fluctuations in pump pressure. Decreased pump rate to 2000 lpm due to minor losses (1.6 m3 over 40 minutes)." "On 2013-05-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3754m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed flow check for 15 minutes due to losses - lost 60 liters static (240 l pr hour)." "On 2013-05-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3794m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 3754 m to 3794 m with 2000 lpm, 156-160 bar, 180 rpm, 18-25 kNm, WOB 6-8 MT, ECD 1.37-1.38 sg. Average ROP: 11.4 m/hr Increased background LCM to 150 kg / stand. Losses gradually decreased to zero." "On 2013-05-01, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3835m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 3794 m to 3835 m with 2000-2350 lpm, 161-216bar, 180 rpm, 18-27 kNm, WOB 9-11 MT, ECD 1.38-1.40 sg. Average ROP: 16.4 m/hr" "On 2013-05-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3900m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3835 m to 3900 m with 2350 lpm, 215-217 bar, 180 rpm, 19-24 kNm, WOB 7-9 MT, ECD 1.39-1.42 sg. Average ROP: 16.3 m/hr." "On 2013-05-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4033m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 3900 m to 4033m with 2350 lpm, 217-219 bar, 180 rpm, 20-24 kNm, WOB 7-11 MT, ECD 1.41-1.46 sg. Average ROP: 14 m/hr. Increased mud weight from 1.28 sg to 1.32 sg. Reamed one stand due to erratic torque readings and increasing ECD." "On 2013-05-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4075m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Performed pipe stretch test. Flushed kill and choke manifold to 1.32 sg oil based mud." "On 2013-05-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4075m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled and orientated 8 1/2' hole from 4075m to 4064m with 2350 lpm, 217-221 bar, 180 rpm, 18-22 kNm, WOB 4-7 MT, ECD 1.45-1.46 sg. Average ROP: 12.4 m/hr." "On 2013-05-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4084m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4064m to 4084m with 2000 lpm, 174-176 bar, 180 rpm, 19-21 kNm, WOB 2-4 MT, ECD 1.45-1.46 sg. Average ROP: 10 m/hr. Drilled with reduced flow due to minor losses (approx 350 l/hr)" "On 2013-05-02, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4162m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4084m to 4162m with 2200 lpm, 209-211 bar, 180 rpm, 19-21 kNm, WOB 1-5 MT, ECD 1.45-1.46 sg. Average ROP: 13 m/hr." "On 2013-05-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4250m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4162m to 4250m with 2200 lpm, 209-211 bar, 180 rpm, 20-23 kNm, WOB 4-8 MT, ECD 1.45-1.46 sg. Average ROP: 15 m/hr." "On 2013-05-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4277m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4250m to 4277m with 2200 lpm, 212-213 bar, 180 rpm, 20-21 kNm, WOB 4-8 MT, ECD 1.46 sg. Average ROP: 13.5 m/hr." "On 2013-05-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4277m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed slow circulation rates." "On 2013-05-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4372m. The activity was categorized as 'drilling -- drill' and lasted for 7.8 hours. Operational details: Drilled and orientated 8 1/2' hole from 4277m to 4372m with 2000-2200 lpm, 181-213 bar, 180 rpm, 19-23 kNm, WOB 2-5 MT, ECD 1.46 sg. Average ROP: 12.3 m/hr." "On 2013-05-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4380m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 4351m to 4380m with 2350 lpm, 220-230 bar, 110 rpm, 21-22 kNm, WOB 5-6 MT, ECD 1.44 - 1.46 sg. Average ROP: 16 m/hr. Intermittent problems with top drive causing decrease in RPM." "On 2013-05-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4446m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4380m to 4446m with 2350 lpm, 230-232 bar, 180 rpm, 18-23 kNm, WOB 4-6 MT, ECD 1.44 - 1.45 sg. Average ROP: 16.8 m/hr. Experienced occational problems with top drive causing decrease in RPM." "On 2013-05-03, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4464m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 4446m to 4464m with 2350 lpm, 230-232 bar, 140-180 rpm, 19-23 kNm, WOB 8-10 MT, ECD 1.44 - 1.45 sg. Average ROP: 7.2 m/hr. Occationally drilled with reduced RPM due to hard stringers." "On 2013-05-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- drill' and lasted for 8.8 hours. Operational details: Drilled and orientated 8 1/2' hole from 4464m to 4562m with 2350 lpm, 232-233 bar, 140-180 rpm, 19-23 kNm, WOB 8-10 MT, ECD 1.44 - 1.45 sg. Average ROP: 11.6 m/hr. Occationally drilled with reduced RPM due to hard stringers. TD reached at 4562m MD." "On 2013-05-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Circulated hole clean with 2300 lpm and 232-233 bar and 130 rpm while reciprocating pipe. Circulated 3 x bottoms up." "On 2013-05-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flow check for 15 minutes - lost 30 liters (120 l/hr). Meanwhile: Performed prejob meeting prior to start relogging and pressure points." "On 2013-05-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4480m. The activity was categorized as 'formation evaluation -- log' and lasted for 7.5 hours. Operational details: Performed relogging of interval 4550m MD to 4480m MD with 2300 lpm, 236 bar, 60 rpm, 19-20 kNm, 1.45 sg ECD and 15 m/hr. Calibrated depth offset to 1.2 m." "On 2013-05-04, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4409m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 4440m MD to 4490m MD. Performed pressure surveys using TestTrak at 4490m, 4468m, 4451m, 4417m and 4409m." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4395m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Performed pressure surveys using TestTrak at 4395m MD." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4393m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.2 hours. Operational details: Relogged interval from 4480m MD to 4393m MD with 2300 lpm, 236 bar, 60 rpm, 19-20 kNm, 1.45 sg ECD and 15 m/hr. Meanwhile: Performed prejob meeting prior to pump out of hole with 8 1/2' bottom hole assembly." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3589m. The activity was categorized as 'drilling -- trip' and lasted for 5.8 hours. Operational details: Pumped out of hole with 8 1/2' bottom hole assembly from 4393m MD to 3589m MD with 1500 lpm and 95 bar." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3058m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly from 3589m MD to 3058m MD." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3058m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Attempted to pull out of hole with 8 1/2' bottom hole assembly from 3058m MD - no go. Observed 20MT overpull. Established circulation at 1800 lpm and 140 bar. Worked string until clear of restrictions." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3008m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly from 3058m to 3008m MD. Observed increasing overpull." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Pumped out of hole with 8 1/2' bottom hole assembly from 3058m MD into 14' casing shoe at 2570m MD with 1100 lpm and 54 bar." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flow check for 15 minutes - well static." "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Serviced drilling equipment" "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2570m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Tested foulty systems in V-ICIS. Meanwhile: Observed 800 liter loss to well during maintanence (400 l/hr)" "On 2013-05-05, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1911m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Pumped slug, pulled out of hole with 8 1/2' bottom hole assembly from 2570m MD to 1911m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 229m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly on 5 1/2' drill pipe from 1911m MD to 229m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 229m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flowcheck for 15 minutes prior to pull 8 1/2' bottom hole assembly through BOP - well static." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: Laid down 8 1/2' bottom hole assembly from 229m MD to deck." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and tidied rig floor." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to making up 8 1/2' bottom hole assembly for VSP." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Made up 8 1/2' bottom hole assembly for VSP." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 413m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly to 413m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 413m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Picked up and made up 6m pup joint." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 816m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 413m to 816m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 816m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Engaged top drive and filled pipe. Installed PS21 slips. Broke off top drive." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1624m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 816m to 1624m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1624m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Engaged top drive and filled pipe. Emptied trip tank and broke off top drive." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2548m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 1624m to 2548m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2548m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Engaged top drive and broke circulation with 2300 lpm and 88 bar. Meanwhile: Performed prejob meeting prior to rig up wireline sheaves in derrick. Rigged up wireline sheaves in derrick." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3436m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 2548m to 3436m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3436m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Engaged top drive and filled pipe. Emptied trip tank." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4528m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 3436m to 4528m MD." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Engaged top drive. Pumped down last stand with 500 lpm and 30 bar. Tagged bottom with 5 MT." "On 2013-05-06, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Staged up pumps to 2300 lpm and 154 bar. Circulated bottoms up with 60 rpm." "On 2013-05-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued circulating bottoms up with 2300 lpm, 154 bar and 60 rpm. Meanwhile: Performed prejob meeting prior to rig up to run VSP." "On 2013-05-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flowcheck for 15 minutes - well static." "On 2013-05-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Removed auto slips and installed master bushings. Rigged up to run wireline through 5 1/2' drill pipe." "On 2013-05-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Picked up and made up wireline toolstring #1 (VSP). Performed prejob tests." "On 2013-05-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 18.5 hours. Operational details: Performed wireline run #1 (VSP) from 4530m MD to 582.9m MD. Moved pipe every hour to check sticky trend. Meanwhile: Troubleshot draworks motor. Performed tests on V-ICIS system. Changed pressure gauges on aft choke. Cleaned and tidied rig floor. Performed general maintanence. Performed prejob meeting prior to rig down wireline run #1 (VSP) and rig up wireline run #2 (Gyro)." "On 2013-05-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Broke out and laid down wireline toolstring #1 (VSP)." "On 2013-05-07, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Picked up and made up wireline toolstring #2 (Gyro). Performed prejob tests." "On 2013-05-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'formation evaluation -- log' and lasted for 14.8 hours. Operational details: Performed wireline run #2 (Gyro) from 145m MD to 4562m MD." "On 2013-05-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Broke out and laid down wireline toolstring #2 (Gyro)." "On 2013-05-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Broke circulation with 2300 lpm and 144 bar. Circulated bottoms up. Meanwhile: Rigged down wireline equipment. Removed wireline sheave from derrick. Installed auto slips." "On 2013-05-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Performed flowcheck for 15 minutes - well static." "On 2013-05-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4407m. The activity was categorized as 'drilling -- trip' and lasted for 5.2 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly from 4562m MD to 4467m MD. Took 5MT overpull at 4467m MD. Attempted to pass restriction several times with maximum 30MT - no go. Attempted to run in hole with 8 1/2' bottom hole assembly with up to 40 MT - no go. Established circulation with 1300 lpm and 54 bar, no losses. Attempted to establish rotation - no go. Applied full string weight, and established rotation. Reamed stand down from 4467m MD to 4482m MD. Attempted to ream stand up several times - no go. Stalled out at 4467m MD. Stopped rotation and circulation and attempted to pull 8 1/2' bottom hole assembly out of hole from 4467m MD - no go. Established rotation with 50 rpm. Got passed restriction. Pulled / reamed out of hole with 8 1/2' bottom hole assembly from 4467m MD to 4407m MD with 1400 lpm, 31 bar, 50 rpm and 16-30 kNm. Observed tight spots at 4468m and 4460m." "On 2013-05-08, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4266m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Lubricated out of hole with 8 1/2' bottom hole assembly from 4407m MD to 4323m MD with 221 lpm and 11 bar." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- trip' and lasted for 9.0 hours. Operational details: Pulled / lubricated out of hole with 8 1/2' bottom hole assembly from 4266m MD to 2550m MD with 200 lpm and 8-9 bar. Observed tight spots at 4230m, 4225m, 4066m-4060m and 3950m with maximum 20 MT overpull." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Filled trip tank." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 410m. The activity was categorized as 'drilling -- trip' and lasted for 4.2 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly from 2550m MD to 410m MD." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 410m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Laid out 6m pup joint. Function tested BOP. Removed PS21 slips." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Pulled out of hole with 8 1/2' bottom hole assembly from 410m. Laid down crossover, near bit stabilizer and bit. Removed totco ring." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Cleaned and tidied rig floor. Prepared to pick up 3 1/2' drill pipe. Changed out dies on iron roughneck." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 293m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Picked up and ran in hole with mule shoe on 3 1/2' drill pipe singles to 293m MD." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 293m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-05-09, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1999m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Ran in hole with cement stinger on 5 1/2' drill pipe from 293m MD to 1999m MD." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Ran in hole with cement stinger on 5 1/2' drill pipe from 1999m MD to 2505m MD." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2571m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Ran in hole with cement stinger from 5 1/2' drill pipe from 2505m MD to 14' casing shoe at 2570,7m MD. Broke circulation with 2500 lpm and recorded pressures (179 bar). Took up and down weights." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2721m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Ran in hole with cement stinger on 5 1/2' drill pipe from 2570m MD to 2721m MD." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2721m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke circulation with 1500 lpm and 70 bar." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3022m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Ran in hole with cement stinger on 5 1/2' drill pipe from 2721m MD to 3022m MD." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 3022m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke circulation with 1500 lpm and 70 bar." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4160m. The activity was categorized as 'drilling -- other' and lasted for 4.8 hours. Operational details: Ran in hole with cement stinger on 5 1/2' drill pipe from 3022m MD to 4160MD. Broke circulation every 500m with 1500 lpm and 70-72 bar." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4160m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: At 4160m MD, observed indication of closed end displacement. Broke circulation with 1500 lpm and 72 bar - ok." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Washed in hole with cement stinger on 5 1/2' drill pipe from 4160m MD to 4562MD with 500 lpm. Tagged TD with 5 MT." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Circulated and conditioned mud prior to cement job at 2500 lpm and 60 bar." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Laid out single drill pipe joint and made up cement assembly. Pressure tested line up to 200 bar." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Pumped 11.8 m3 of 1.50 sg spacer. Mixed and pumped 10 m3 of 1.90 sg cement slurry. Displaced the cement to the rig floor with 890 l of drill water. Reset stroke counters. Pumped 2.8 m3 of 1.50 sg spacer. Displaced the cement with 40.6 m3 (1833 strokes) of 1.32 sg OBM. Underdisplaced with 2.5m3. Rotated with 20 rpm and 15 kNm during displacement." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Laid out cement assembly and picked up and made up single drill pipe joint." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4367m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 4562m MD to 4367m MD. Observed 20MT overpull at 4450m MD." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4367m. The activity was categorized as 'drilling -- other' and lasted for 2.8 hours. Operational details: Dropped 2 wiper balls and circulated string clean with 2500 lpm. Continued circulating out excess cement and spacer with 2500 lpm. Diverted 77m3 contaminated mud and spacer to slop." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4367m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Laid out single drill pipe joint and made up cement assembly. Pressure tested line up to 200 bar." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4367m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Pumped 10 m3 of 1.50 sg spacer. Mixed and pumped 10 m3 of 1.90 sg cement slurry. Displaced the cement to the rig floor with 890 l of drill water. Reset stroke counters. Pumped 2.8 m3 of 1.50 sg spacer. Displaced the cement with 38.6 m3 (1742 strokes) of 1.32 sg OBM. Underdisplaced with 2.5m3. Rotated with 20 rpm and 15 kNm during displacement. Diverted 40m3 contaminated mud and spacer to slop." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4367m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Laid out cement assembly and picked up and made up single drill pipe joint." "On 2013-05-10, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4087m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger on 51/2' drill pipe from 4367m MD to 4087m MD." "On 2013-05-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4023m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 4087m MD to 4023m MD." "On 2013-05-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4023m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Dropped 2 wiper balls and circulated string clean with 2500 lpm. Continued circulating out excess cement and spacer with 2500 lpm." "On 2013-05-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2571m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 4023m MD to 2571m MD." "On 2013-05-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2310m. The activity was categorized as 'interruption -- wait' and lasted for 2.2 hours. Operational details: Waited on cement. Meanwhile: Pulled out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 2571m MD to 2310m MD." "On 2013-05-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2310m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Waited on cement. Meanwhile: Cleaned and cleared rig floor prior to BOP test." "On 2013-05-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2310m. The activity was categorized as 'interruption -- wait' and lasted for 12.2 hours. Operational details: Waited on cement. Meanwhlie: Performed prejob meeting prior to pick up and make up BOP test tool. Removed PS21 slips and installed master bushings. Picked up and made up BOP test tool, removed protective tape and inspected seals. Ran in hole with BOP test tool on 5 1/2' drill pipe to wellhead at 138m MD. Displaced riser and surface lines to sea water. Pressure tested BOP to 345 bar. Pressure tested standpipe manifold to 345 bar. Displaced BOP to surface to 1.32 sg OBM. Pulled out of hole with BOP test tool on 5 1/2' drill pipe from 138 m MD. Broke out and laid down same. Troubleshooting on top drive encoder. Function tested same. Function tested 3 1/2' auto slips. Performed general maintanence and housekeeping." "On 2013-05-11, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2310m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.8 hours. Operational details: Pressure tested IBOPs to 345 bar." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2310m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: Pressure tested IBOP's to 345 bar." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2970m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Ran in hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 2310m MD to 2970m MD." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2970m. The activity was categorized as 'drilling -- other' and lasted for 4.5 hours. Operational details: Broke circulation and staged up to 3000 lpm and 248 bar. Diluted mud weight from 1.32 sg to 1.28 sg." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4044m. The activity was categorized as 'drilling -- other' and lasted for 3.5 hours. Operational details: Ran in hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 2970m MD to 4044m MD. Broke circulation every 500m." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4104m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Washed in hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 4044m MD to 4104m MD with 200 lpm and 20 bar. Tagged hard cement at 4104 with 10MT." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 4104m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Rigged up mud bucket prior to pulling out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2970m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 4104m MD to 2970m MD." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2970m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Spotted 1.32 sg hi-visc pill from 2970m MD to 2770m MD." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 2970m MD to 2770m MD." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Circulated and conditioned mud prior to start cement job with 2250 lpm and 133 bar. Meanwhile: Performed prejob meeting prior to start cement job." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Racked back one stand of 5 1/2' drill pipe. Cleaned and tidied rig floor." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Picked up and made up one single joint and cement assembly to top drive." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Pressure tested cement line to 200 bar and verified line up. Pumped 20 m3 of 1.50 sg spacer. Mixed and pumped 13.5 m3 of 2.00 SG cement slurry. Displaced the cement to the rig floor with 790 l of drill water. Pumped 3.3 m3 of 1.50 SG spacer. Displaced the cement with 24 m3 (1083 strokes) of 1.28 sg OBM." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2569m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Broke out and laid out cement assembly and one single drill pipe joint. Pulled out of hole with 3 1/2' cement stinger and 5 1/2' drill pipe from 2770m MD to 2569m MD." "On 2013-05-12, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2569m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Installed two sponge balls and circulated out spacer and excess cement at 2569m MD with 2500 lpm, 162 bar and 60 rpm." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2569m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: Circulated out spacer and excess cement at 2569m MD with 2500 lpm, 162 bar and 60 rpm." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 291m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger on 5 1/2' drill pipe from 2569m MD to 291m MD." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 291m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed flowcheck prior to pull 3 1/2' cement stinger through BOP - well static." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 291m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed out PS21 slips and installed 3 1/2' auto slips. Broke out 3 1/2' x 5 1/2' crossover and laid down. Changed out die carriers and elevator inserts." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Pulled out of hole with 3 1/2' cement stinger from 291m MD and racked back same. Broke out and laid down mule shoe." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Changed to 5 1/2' handling equipment. Cleaned and tidied rig floor." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed prejob meeting prior to pick up and make up 8 1/2' bottom hole assembly." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: Picked up and made up 8 1/2' bottom hole assembly to 40m MD. Uploaded MWD and installed radioactove sources. Picked up and made up 8 1/2' bottom hole assembly from 40m MD to 196m MD." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 993m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 196m MD to 993m MD." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 993m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Engaged top drive and filled pipe. Established circulation with 2200 lpm and 123 bar." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 993m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Shallow tested MWD." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 993m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Displaced kill and choke lines to 1.28 sg OBM." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1354m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 993m MD to 1354m MD." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1354m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Emptied trip tank." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1609m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 1354m MD to 1609m MD." "On 2013-05-13, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1609m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Performed slip and cut of drill line." "On 2013-05-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1609m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: Performed slip & cut of drill line." "On 2013-05-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1609m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Cleaned and cleared rig floor. Recalibrated block." "On 2013-05-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 1609m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Tested crownomatic. Serviced drilling equipment prior to run in hole and kicking off to F-11 A." "On 2013-05-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Ran in hole with 8 1/2' bottom hole assembly from 1609m MD to 2536m MD." "On 2013-05-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2573m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Washed down last stand with 1600 lpm and 90 bar. Tagged hard cement at 2573m MD with 10MT." "On 2013-05-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2578m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled hard cement and clean out rat hole from 2573m MD to 2578m MD with 1600 lpm, 120 bar and 60 rpm." "On 2013-05-14, at Well NO 15/9-F-11, a drilling event occurred at a depth of 2586m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Kicked off to F-11 A by drilling from 2578m MD to 2586m MDwith 1800 lpm, 120 bar and 60 rpm. 50% cement / formation in returns verified at 2586m MD. ****Transferred operations to F-11 A****" "On 2007-06-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.0 hours. Operational details: Installed hatches in wellhead module. Removed scaffolding in moonppol. Removed cantilever walkway. Removed conflicting scaffolding. Relocated goods/carriers on maindeck to give way for cantilever and gangway when skidded to F-12." "On 2007-06-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to skidding rig." "On 2007-06-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded rig from F-4 to F-12." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.8 hours. Operational details: Removed covers/bushings on slot F-12 in wellhead module." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up 36' hole opener BHA." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Made up 36' hole opener BHA." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Had problems with PRS when picking assembly from derrick. Troubleshot PRS." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 85m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued to m/u and RIH with 36' hole opener BHA." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 86m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued to RIH with 36' hole opener BHA." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 86m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to technichans working on TDS." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 86m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Performed dropped object checks on TDS." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 86m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Calibrated MWD depth sensor towards block positions." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 86m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Performed dummy connection with TDS. Adjusted make up sequence on TDS to avoid jamming torque wrench. Mærsk maintenance hours." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 86m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to repairs on TDS. Mærsk maintenance hours." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 86m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Performed repair work on TDS. Mærsk maintenance hours." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued to RIH with 36' hole opener on 5 1/2' HWDP. Tagged seabed at 145,2 m MD RT." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Washed down from seabed to 149 m MD at 900 lpm with 36' hole opener. ROV observed centralizer guide bushing land in template funnel. Parked ROV in top hat before starting to rotate." "On 2007-06-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: Drilled 36' hole section from 149 m to 221 m MD. Drilling parameters : Rotation 80 rpm / WOB 3 MT / Flow 4500 lpm / Torque 4-9 kNm. Swept hole clean with 15 m3 his-vis on conncetion." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 250m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drillig 36' hole section from 221 m to 250 m MD. Drilling parameters : Rotation 80 rpm / WOB 3-5 MT / Flow 4500 lpm / Torque 6-13 kNm. Swept hole clean with 15 m3 his-vis on conncetion." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 258m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drilling 36' hole section from 250 to 258 m MD. Drilling parameters : Rotation 80 rpm / WOB 5 MT / flow 4500 lpm / Torque 3-7 kNm." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 258m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated hole clean at 4500 lpm / SPP 94 bar. Took final survey on TD - 0,15 deg. Swept hole with 25 m3 hi-vis pumping at 4500 lpm." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 258m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Displaced well to 1,40 sg WBM pumping at 4250 lpm. Pumped at total of 105 m3 WBM." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 36' hole opener BHA on 5 1/2' HWDP to 150 m MD." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Topped up well by pumping 5 m3 of 1,40 sg WBM." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Continued to POOH with 36' hole opener BHA. Racked back 5 1/2' HWDP and DC." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Broke out an laid down MWD. Laid out 36' hole opener BHA, lifted same to maindeck for backload." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Performed FG inspection of TDS and derrick." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging up 30' conductor handling/running equipment." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Rigged up 30' conductor handling/running equipment." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held toolbox talk prior to running 30' conductor. Deck crew recieved helicopter." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Halted operations due to PORT FWD crane down." "On 2007-06-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 96m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Ran 30' conductor shoe joint, 6 x intermediate joints and ST-2 x RL-4 x-over from RT to 96 m MD. Checked float - ok." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 96m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Removed 30' elevator. Removed long bails. Installed short bails and 5 1/2' elevator. Brought 30' conductor housing to catwalk cradles." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 96m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up 30' conductor housing with handling CART. Made up RL-4 connection using manual tongs to 35 000 ft lbs. Engaged anti rotation dogs. Ran in with 30' conductor and installed top up pipe on XMT deck from 25 m below ML." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed C-plate in rotary and landed 30' conductor housing in same." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out and laid down handling CART from 30' conductor housing. Filled 30' conductor with water. Rigged up C-plate, bowl and slips for running 4 3/4' aluminium inner string inside 30' conductor." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran 4 3/4' aluminium inner string inside 30' conductor down to 20 m below RT." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued to run 4 3/4' aluminium inner string inside 30' conductor down to 91 m below RT. Installed centralizers on joint #3 and #6. Rigged down 4 3/4' handling equipment." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to installing CART in 30' conductor housing." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Installed CART in 30' conductor housing with 5 lefthand turns. Oceaneering installed inclinometer on CART bracket. Verified filler valve open." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 126m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with 30' conductor on 5 1/2' HWDP. Installed top up pipe along X-over and conductor housing. Hooked up UWG cement hose to top up pipe. Installed ROV plugs on Centralizer deck." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continued to RIH with 30' conductor on 5 1/2' HWDP. Stabbed into template. Broke circulation and observed for return with ROV - bad visibility. Weight of string in water 105 MT." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 225m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued to RIH with 30' conductor. Observed up to 10 MT drag at 225 m MD." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Broke circulation and washed down with 30' conductor from 225 m to 251 m MD. Pumped at 200 lpm / 9 bar SPP. Installed cementing stand. Checked datum mark 113,25 m from top conductor housing to machined ring on Centralizer deck - ok." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held prejob meeting prior to cementing 30' conductor." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Made up surface cement lines to cement stand. Tested lines against lo-torqe valve to 200 bar / 5 min - ok. Circulated at 2500 lpm / SPP 12 bar. ROV checked for leakage in plugs on 30' conductor housing - ok. Inserted hotstab with ROV, actuated centralizer dogs in template funnel using minireel hydraulic supply from surface." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pumped 103 m3 of 1,52 sg X-lite cement slurry with cement unit. Pump pressure during displacement 15 bar. Displacement rate 900 lpm. Hook weight fell from 115 MT to 110 MT throughout cement job." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced cement with seawater at 1200 lpm. Pressure relatively steady around 17 bar. Pumped a total of 8,5 m3 leaving theoretical TOC at 247 m MD inside 30' conductor." "On 2007-06-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Waited on cement to set up. Meanwhile : -Flushed and washed cement unit -Brought tensioning system parts to Centralizer deck -Broke out and laid down Drillcollar -Prepared for running LP riser" "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Waited on cement to set up. Meanwhile : -Prepared and tested lines for top up job -Brought tensioning system parts to Centralizer deck" "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held toolbox talk prior to pumping operation. Assessed cool cement sample - still fingersoft. Lined up cement unit to UWG hose and top up pipe. Circulated at 30 lpm to check for potential flow bypass above cement on lower UWG shoe. Pressure built up to 5 bar with linear build, maintained pressure for 5 min, no pressure drop. Volume pumped 193 liter. Halted operation, bled back pressure and continued wating on cement to set up." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Restarted pumping operation to check cement shoe and burst disk on top up pipe. Pumped down cement unit and top up pipe. Pressured up to 53 bar / 189 l, burst disk at 14 m below ML / 159 m MD ruptured." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Attempted to do circulation test through UWG cement hose/ top up pipe. Got alarm on overpressured cement unit. Released pressure, but control screen froze up." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Troubleshooting on Halliburton control screen. Unable to sign out alarms / system freeze." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: By manual operation of cement unit. Stepped up rate through cement hose / top up pipe to 500 lpm, obtained same pressure drop as previously i.e. 50 bar at 500 lpm indicating open flow above bursted disk at 14 m below ML / 159 m TVD." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held pre job meeting. Prepared for cement job. Got ROV in position to operate centralizing rods in funnel, shifted handles and pressured up thorugh minireel to retract rods - ok. Started mixing cement." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed remedial cement job. Pumped 10 m3 1,56 G-cement slurry. Pump pressure during cementing 70 bar. Pump rate 500 lpm. Displaced cement down cement hose and top up pipe with 1,1 m3 SW." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke cement hose in moonpool, inserted cement hose release ball. Let ball drop by gravity. Pressured up on cement unit and released cement hose. Flushed through manifold and cement hose. Flushed and cleaned cement unit." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pulling CART." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released CART from 30' conductor housing with 5 righthand turns. Readings on inclinometer before release: Pitch 0,25 / Roll 0,021" "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out cement stand and laid out same. Pulled CART clear of template." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped sponge for cleaning the 5 1/2 HWDP landing string." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held prejob/information meeting for running LP drilling riser. Whole crew attended." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to pulling CART." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired hydraulic leak on TDS." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH with CART on 5 1/2' HWDP. Laid out CART. Rigged handling equipment for 4 3/4' inner string." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pulling 4 3/4' aluminium cement stinger." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with 4 3/4' aluminium cement stinger and centralizers, laid down on pipe deck." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleaned and tidied drillflloor. Removed handling equipment for 30' condcutor and innerstring." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to installing cradles in HTS." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed cradles on HTS. Installed protector busing in Tensioner deck." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to installing riser spider." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Removed master bushing and installed riser spider. Installed hydraulic lines and function tested spider. Installed protector bushing and tension ring in Centralizer deck." "On 2007-06-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up Stress joint / DCI joint - 1st double, by simultaneous lift by deckcrane and TDS. Landed double in spider. Removed handling flange and installed guide rods on flange, installed gasket ring. Picked up 2nd double and landed on flange. Made up nuts according to Bandak procedure." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Continued making up flange according to Bandak procedure. Removed hatch covers on slot #11 and #13. Rearranged sheaves for guidewires and ran guidewires to Centralizer deck." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Ran in with LPDR to 30 m MD, stopped when guide sling in level with scaffolding below Centralizer deck. Ran out guidewire and hooked guidewires into slings above RL-4 connector. Ran aft guidewire and hooked onto eagle clamp on template by ROV. Ran in to 80 m MD and landed LPDR in spider. Strilhav on near standby from 01.30 to 04.00 due to personnel working on scaffolding deck below Centralizer deck." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Picked up 3rd double. Installed guide rods on flange, installed gasket ring. Landed double on flange. Made up nuts according to Bandak procedure. RIH with LPDR to 80 m MD. Removed handling flange. ROV hooked up FWD guidewire to eagle clamp on template." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up splash zone / upper pup - 4th double. Installed guide rods on flange, installed gasket ring. Landed double on flange." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Continued to make up 3rd and 4th double LPDR according to Bandak procedure. RIH with LPDR to 105 m MD, landed on spider, removed handling tool." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up tensioner joint - last single. Installed guide rods on flange, installed gasket ring. Landed tensioner joint on flange in riser spider. Made up flange according to Bandak procedure. RIH with LPDR to 122 m MD." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up landing string." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up to joints/connections in landing string to 67500 Nm, applied threadlock." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up landing string to LPDR running tool / flange, applied threadlock. Removed riser spider and installed master bushing." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Ran in with LPDR on landing string to 2 m above 30' conductor housing. Tensioned up guidewires. While observing with ROV, stabbed LPDR RL-4 connector onto 30' conductor housing. Using rig tongs, made up RL-4 connection to 40650 Nm with CCW rotation. Performed overpull test with 10 MT and maintained overpull." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to assembling tensioning system." "On 2007-06-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.0 hours. Operational details: Elevated Tension ring with chain hoists on Centralizer deck. Installed brass bushing and Boat collision stool on Centralizer deck. Meanwhile=>During ROV inspection on 30' conductor housing, observed that steel band for conductor ROV plugs was misalligned. Two ringbolts were missing. Assessed situation, conferred with shore and made contingency plan for getting the band back in place. Moved steelband back in place using ROV manipulator arm - obtained good fit on bolt holes and verified that steelband still was thight." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Installled Contact ring and tensioner ring assembly on Centralizer deck. Meanwhile performed repair activities on conductor housing steelband. Welded/prepared threaded T- bars for replacing lost eyebolts on steelband. Dove ROV, inserted and made up threaded T-bars in steelband / ROV plug boltholes. Cut slings on guidewires using hydraulic cutter. Retrieved FWD and AFT guidewire. Installed and secured hatches on F-11 and F-13 openings on Centralizer deck, removed scaffolding. Tided Centralizer deck." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Elevated and made up contact ring to serrated area on tensioning joint. Made up Tensioner ring assembly and made up to Tension ring. Mounted 2 tensioning cylinders to tensioning assembly." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.2 hours. Operational details: Continued to work on tensioning system on Centralizer deck. Mounted tensioning cylinders. Made up nuts on Contact ring. Tested hydrualic system. Tranferred tension to tensioning cylinders by applying 90 bar pressure on each equivalent to 150 MT total tension." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Slacked off weight on block. Broke out Tension joint running tool/flange on Tensioning deck." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pulling LPDR running tool/flange." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with landing string, broke and laid down same. Broke out running tool/flange." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Installed cradles on HTS for handling overshot joint. Picked up overshot joint and landed off on top of LPDR Tension joint. Torqued up bolts in overshot." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Made repairs on TDS. Serviced TDS counterbalance and rotating head. Meanwhile installed new actuator on flowline isolation valve." "On 2007-06-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Rigged TDS with long slings for running diverter. Removed master bushing. Lifted diverter into diverter housing." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Secured overshot joint with tugger in moonpool due to movements in same. Landed diverter on overshot joint. Made up diverter to overshot joint." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Changed dye block retaining plate on TDS. Meanwhile worked to function flowline isolation valve." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Filled conductor with seawater. Observed leakage above diverter (environmental barrier). Meanwhile worked to function flowline isolation valve." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held handover meeting on drillfloor. Held toolbox talk prior to picking up 26' drillout BHA." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 9m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Picked up and installed 12 1/4' x 17 1/2' x 26' drillout BHA. Gauged bit. Meanwhile worked to function flowline isolation valve." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pick up and make up 9 3/4' DC. Meanwhile worked to function flowline isolation valve." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Continued making up 26' drillout BHA. RIH with 26' drillout BHA to 180 m MD. Meanwhile worked to function flowline isolation valve." "On 2007-06-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 180m. The activity was categorized as 'interruption -- other' and lasted for 15.0 hours. Operational details: Worked to function flowline isolation valve. Meanwhile : -Changed conveyer belt on HTS -Treated pit #5,#6 and #7 with H2S scavanger -Laid out HPDR on pipedeck" "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 180m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Worked to function flowline isolation valve. Meanwhile . -Preparing for making up HPDR in doubles on pipedeck -Transferred slop from pit #6 to DCI holding tank" "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 180m. The activity was categorized as 'interruption -- other' and lasted for 8.0 hours. Operational details: Function tested flowline isolation valve from Koomey unit. Could not operate valve from BOP panel due to lacking signal from PLC. Managed to operate flowline isolation valve manually. Meanwhile . -Worked on TDS and flowline actuator. -Performed daily maintenace, PMs and housekeeping. -Emptied flowline to trip tank. -Greased flowline isolation valve periodically during testing." "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held tool box meeting prior to drilling out shoe track. Focused on potential for stuck pipe." "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 250m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 26' hole opner BHA from 180 m to 222 m. Washed down from 222 m with 2000 lpm, 12 bar. Tagged cement at 250 m with 3 ton. Up weight 94 t/ Down weight 97 t." "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 250m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled cmt/shoe track with 26' hole opner BHA; 3000 lpm, 50 rpm and 1-3 ton wob. Picked bit off bottom and stopped pumps." "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 250m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Function tested diverter system. Ran diverting sequence on port and aft overboard lines from BOP panel. Verified visually that diverter element closed, flowline isolation valve closed and diverter line valve opened." "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 258m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Continued to drill cmt/shoe track from 250 m until 26' hole opener was out of 30' conductor shoe; 3000 lpm, 50 rpm and 1-3 ton wob. Reamed shoe track every 1-2 m. Pumped 15 m3 1.12 sg hi-vis pill and circulated out same. Noticable increase in cuttings observed." "On 2007-06-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 260m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 2 m new formation with 26' hole opner BHA; 3000 lpm, 55 rpm and 1 ton wob. Reamed rate hole and shoe track." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 261m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 1,5 m new formation with 26' hole opner BHA; 3000 lpm, 55 rpm and 0.5-1 ton wob. Reamed rat hole. Pumped 15 m3 1.12 sg hi-vis pill and circulated out same. Meanwhile held tool box meeting for manual handling of BHA." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Pulled through shoe track without rotation to verify no restrictions and continued POOH to 141 m." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 141m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Malfunction of forward PRS. Trouble-shooted same and found failure on proximity switch." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued POOH with 26' HO BHA and racked back same." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Held tool box meeting prior to removing master bushing and diverter inserts. Removed inserts." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued POOH with 26' HO BHA and racked back same." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH with 26' HO BHA from 29 m to 8 m and racked back same. Held tool box meeting prior to POOH with 12 1/4' x 17 1/2' x 26' hole opener assembly. Removed master bushing and LO 26' HO BHA. Cleared rig floor." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Held pre-job meeting. PU and RIH with 8 1/2' pilot hole BHA to 32 m." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Held tool box meeting prior to installing radioactive source. Barried off wellhead, moonpool and rigfloor. Installed radioactive source into ADN according to Schlumberger procedure." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 225m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: Continued to PU and RIH with 8 1/2' pilot hole BHA from 32 m to 225 m. Meanwhile recovered ROV to surface to repair camera." "On 2007-06-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 112m. The activity was categorized as 'drilling -- wait' and lasted for 6.5 hours. Operational details: Raw water pumpe failed and left rig with only 1 out of 3 pumpes available. Due to the criticality of the pump delivering firewater, cooling water etc the drilling operation is postphoned until the pump is replaced. -Meanwhile held tool box meeting to install diverter elements. Removed master bushing and replaced torn 22' outer diverter elements by new 18' elements. -Meanwhile held tool box meeting prior to POOH. POOH with 8 1/2' BHA from 212 m to 32 m. -Meanwhile cleared rig floor before handling radioactive sources. Removed batteries. - Meanwhile continued POOH to 17 m." "On 2007-06-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 8m. The activity was categorized as 'drilling -- wait' and lasted for 4.0 hours. Operational details: Waited on boat to arrive with raw water pump. Meanwhile continued to LO BHA from 17 m to surface. Cleaned and cleared rig floor of excess equipment. Lowered foldable finger board, changed inserts in fox hole and arranged equipment in set back prior to PU 3 1/2' DP. Held tool box meeting prior to MU 3 1/2' DP." "On 2007-06-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 8m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: MU and RB 3 1/2' DP. Changed dies in aft PRS. Meanwhile started installation of raw water pump." "On 2007-06-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: MU and RB 3 1/2' DP. Meanwhile trouble-shooted raw water pump failure and performed rig maintenance, housekeeping and monitored well on trip tank. Found leak rate of 200 l/hour." "On 2007-06-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 12.0 hours. Operational details: Waiting on trouble-shooting of raw water pump failure. -Meanwhile removed master busing, installed 18' and 10' diverter inserts and re-installed master bushing. -Meanwhile worked with mechanic on TDS. -Meanwhile observed leak rate of 250 l/hour. Found leaking valve on flowline valve. Actuator misaligned and unable to fully close flowline -Meanwhile dumped pit 6 (active) and filled with fresh seawater. Dressed all 6 shakers with 20/80 mesh screens." "On 2007-06-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 6.0 hours. Operational details: Waiting on trouble-shooting of raw water pump failure. Meanwhile worked on flowline valve and actuator and stopped observed leakage." "On 2007-06-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 13.0 hours. Operational details: Waiting of raw water pump repair. -Meanwhile performed rig maintenance, performed dropped object survey punch items and prepared equipment for 26' section. - Meanwhile monitored well on trip tank. Loss rate of approx. 100 l/hour recorded. - Meanwhile performed man ride service on TDS and 2 PRS and changed out valve on diverter system. -Meanwhile had derrick inspection." "On 2007-06-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 246m. The activity was categorized as 'drilling -- wait' and lasted for 5.0 hours. Operational details: Waiting of raw water pump repair. Meanwhile PU and RIH with 8 1/2' pilot hole BHA to 246 m. Schlumberger fitted fresh batteries and loaded RA source." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- wait' and lasted for 0.2 hours. Operational details: Waiting of raw water pump repair. Meanwhile PU and RIH with 8 1/2' pilot hole BHA from 246 to 251 m." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Had pre-job meeting with all personnel on shallow gas procedure. Performed shallow gas drill inside shoe at 251 m. Pumped 900 lpm, 15 bar and operated diverter bag and observed flow being re-directed through port overboard line. Switched between pits on the fly." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Pumped 27m3 1.60 sg mud at 2000 lpm, 110 bar and displaced out of bit using seawater. Flow checked well for 1 hour. Had stable loss rate of 120 l/hour eqvivalent to the loss rate monitored on the trip tank prior to the FIT. Picked up 1 stand and circulated out upper part of 1.60 sg mud, 2000 lpm and 84.5 bar. RIH with 1 stand and circulated out remaining 1.60 sg mud." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 296m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled 8 1/2' pilot hole BHA from 261.4 m to 296 mMD, 2000 lpm, 89 bar, 60 rpm, 1-4 kNm, 1-3 MT wob, ECD 1.19 SG, ROP 9 m/hr. BHA WT 23 MT. WT below jar 15 MT." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: PU off bottom and circulated due to riser leak. Pumped out to shoe from 296 m to 251 m, 890 lpm and 10 rpm. Located leak to be in wellhead connector, 70-80 l/hr." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Flow checked well over trip tank while waiting on decision. Leakage stopped and well flow checked ok. Meanwhile performed general maintenance and houskeeping." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 399m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: RIH with 8 1/2' pilot hole BHA from 251 to 290 m. MU TDS and washed down from 290 m to 296 m. Drilled 8 1/2' pilot hole from 296 m to 399 mMD, 2000 lpm, 90-98 bar, 60-120 rpm, 1-4 kNm, 1-3 MT wob, ECD 1.20 SG, ROP 15-20 m/hr." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 399m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated and reciprocated btms up, 2000/2250 lpm, 100/114 bar, due to rapide increase in ECD to 1.23 SG. Diluted and conditioned mud from 1.14 sg to 1.12 sg." "On 2007-06-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 415m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8 1/2' pilot hole from 399 m to 415 mMD, 2250 lpm, 112 bar, 120 rpm, 2-3 kNm, 1-3 MT wob, ECD 1.21-1.23 SG, ROP 10-46 m/hr, Inc 0.46 deg." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 467m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 8 1/2' pilot hole from 415 m to 467 mMD, 2272 lpm, 116 bar, 120 rpm, 2-3 kNm, 1-3 MT wob, ECD 1.23-1.25 SG, ROP 36 m/hr." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 467m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Circulated and reciprocated btms up, 2272 lpm, 116 bar, due to rapide increase in ECD to 1.27 SG. Diluted and conditioned mud from 1.15 sg to 1.12 sg." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 473m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 8 1/2' pilot hole from 467 m to 473 mMD, 2272 lpm, 116 bar, 120 rpm, 2-3 kNm, 1-2 MT wob, ECD 1.25 SG, ROP 37 m/hr. Observed gain of 1 m3 in active. PU off btm and flow checked well static for 15 min. Ok." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 476m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated btms up, 2272 lpm, 116 bar. No gas observed. Meanwhile diluted and conditioned mud to 1.12 sg." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 525m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 8 1/2' pilot hole from 476 m to 525 mMD, 2272 lpm, 116 bar, 120 rpm, 2-3 kNm, 1-2 MT wob, ECD 1.23 SG. Reduced ROP from 36 m/hr to 30 m/hr at 500 m according to program." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 618m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' pilot hole from 525 m to 618 mMD, 2250 lpm/115 bar, 120 rpm/1-6 kNm, 2-15 MT wob, ECD 1.21-1.23 SG. Limited 30 m/hr according to program. ROV monitored wellhead connector." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 578m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Reamed full stand and circulated well clean, 2250 lpm 115 bar. Racked back one stand." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 578m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: MU TDS, rotated 10 rpm and flow checked well. Total loss 140 l over 1.5 hr. Meanwhile checked rollers and dies on AFT PRS." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 578m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Prepared to wash std down. Unable to open flowline isolation valve." "On 2007-06-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'interruption -- other' and lasted for 9.0 hours. Operational details: Trouble-shooted and repaired flowline isolation valve. Meanwhile POOH from 578 m to shoe at 251 m." "On 2007-06-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Trouble-shooted and repaired flowline isolation valve. Meanwhile performed general housekeeping." "On 2007-06-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'interruption -- other' and lasted for 9.5 hours. Operational details: Repaired flowline isolation valve. Meanwhile performed general maintenance and housekeeping. Performed derrick inspection and monitored well on trip tank. Stable loss rate 170 l/hr (LPDR connector)." "On 2007-06-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 618m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Washed down from 251 m to 618 m, 2250 lpm/109 bar. No fill." "On 2007-06-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 618m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Had pre-job meeting with new night crew on shallow gas procedure and function tested flowline isolation valve 5 times." "On 2007-06-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 685m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 8 1/2' pilot hole from 618 m to 685 m, 2250 lpm/114 bar, 120 rpm/1-3 kNm, 1-3 MT wob, ECD 1.21-1.24 SG. Observed losses, 3 m3/15 min at 655 m. Circulated with reduced flow, 1800 lpm. Increased flow rate to 2250 lpm and observed loss of 200 l/min. Total loss was 10 m3." "On 2007-06-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 780m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' pilot hole from 685 m to 780 m, 2250 lpm/115 bar, 120 rpm/1-4 kNm, 1-3 MT wob, ECD 1.21-1.25 SG. Circulated and reamed one std every 3 hours due to high ECD reading of 1.27 SG. No loss observed." "On 2007-06-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 870m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: Drilled 8 1/2' pilot hole from 780 m to 870 m, 2250 lpm/117 bar, 120 rpm/1-3 kNm, 3-4 MT wob, ECD 1.25 SG." "On 2007-06-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 870m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated hole clean prior to drilling through Utsira formation, 2250 lpm/113 bar, 120 rpm/1-3 kNm." "On 2007-06-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 890m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continue to drill 8 1/2' pilot hole from 870 m to 890 m, 2250 lpm/117 bar, 120 rpm/1-3 kNm, 0-6 MT wob, ECD 1.25 SG. Observed increasing WOB from 880 to 882 followed by no WOB from 882 m to 886 m." "On 2007-06-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 890m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated hole clean, 2250 lpm/113 bar, 120 rpm/1-3 kNm." "On 2007-06-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 890m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Function tested flowline isolation valve 5 times. Displaced well to seawater, 2250 lpm/102 bar, 100 rpm/1-3 kNm. Flow checked well and observed loss of 500 l/hr. Observed increasing leak rate on connector using seawater." "On 2007-06-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 941m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Pumped 10 m3 hi-vis pill and started drilling 8 1/2' pilot hole from 890 m to 941 m2250 lpm/105 bar, 120 rpm/1-3 kNm, 0-1 MT wob, ECD 1.12 - 1.20 SG . Pumped 10 m3 hi-vi pills according to program. Had to back-ream 1 std every 5-10 m due to high ECD readings. Meanwhile decided to displace well to WBM." "On 2007-06-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 941m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Prepared for connection at 941 m and had 10 MT WOB at 934 m, 120 rpm. Slowed down to 30 rpm and re-ran in and got 5 MT WOB at 934 m (had 0-1 MT WOB while drilling this section). Pulled back to 910 m and circulated and swept 2 x 5m3 hi-vis pills. Took time-out to discuss further action. Meanwhile had boat delivering drillwater for mixing mud." "On 2007-06-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 941m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Mixed 1.08 sg mud and displaced well to same, 2250 lpm/105 bar, 30 rpm/1-3 kNm." "On 2007-06-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1178m. The activity was categorized as 'drilling -- drill' and lasted for 14.0 hours. Operational details: Drilled 8 1/2' pilot hole from 941 m to 1178 m, 2250 lpm/111 bar, 120 rpm/1-5 kNm, 1-2 MT wob, ECD 1.14-1.20 SG. Reamed each stand. Took weight at 978 m, 1027 m, 1040 m and 1060 m, while reaming. Worked through tight spots and continued drilling. Observed max gas reading of 0.6%. Stringer at 1002-1003 m." "On 2007-06-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1178m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Rig ESD system had shut-down. Managed to rotate string 10 rpm and pump 200 lpm with cement unit." "On 2007-06-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1178m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Reamed 1 std and circulated btms up, 2250 lpm/101 bar, 125 rpm/1-5 kNm. Lost 2 m3/hr over shakers due to high amount of cuttings." "On 2007-06-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1178m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Waiting on Geoservices to have their sensors reading data. Meanwhile reamed and circulated 2250 lpm/101 bar." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1178m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Waiting on Geoservices to have their sensors reading data. Meanwhile reamed and circulated 2250 lpm/101 bar." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1262m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 8 1/2' pilot hole from 1178 m to 1262 m, 2250 lpm/105 bar, 125 rpm/2-3 kNm, 1-4 MT wob, ECD 1.19-1.28 SG. Reamed each stand. Reamed and circulated when experienced high ECD readings." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1353m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' pilot hole from 1262 m to 1353 m, 2250 lpm/108 bar, 125 rpm/2-5 kNm, 1-4 MT wob, ECD 1.19-1.28 SG. Reamed each stand. Reamed and circulated when experienced high ECD." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1353m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated 2 x btms up, 2250 lpm/108 bar, 125 rpm/2-5 kNm." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1353m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow check well prior to displace well to 1.40 sg WBM. Meanwhile held tool-box talk for displacement." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1353m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Displaced well to 50 m3 of 1.40 sg WBM, 1200 lpm/8 bar, 80 rpm/1-4 kNm. Max ECD 1.21 sg." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 290m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: POOH with 8 1/2' BHA from 1353 m to 294 m. Observed 2 MT max drag. Meanwhile placed cuttings funnel on F-4 using moonpool tugger." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 290m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 13 m3 of 1.40 sg WBM at 290 m, 900 lpm/11 bar, 10 rpm/1-3 kNm, to displace lower part of 30' conductor to heavy mud." "On 2007-06-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: POOH with 8 1/2' BHA from 294 m to 32 m. RB 5.5' HWDP and 6 3/4' DC." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: POOH and LO 8 1/2' BHA from 32 m to OOH. Removed RA source from MWD tool and dumped memory data." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Cleared and cleaned drill floor. Prepared removal of diverter. Installed sadle and cradle on HTS. Held tool-box talk with crew. Installed lifting bolts on diverter." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Removed broken stud from diverter locking dog. Installed new lifting bolt. Bled off pressure in tension system from 90 bar to 60 bar and observed easier movement of locking dog." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Held tool-box meeting prior to lifting diverter to rig floor. Lifted with weight of diverter (10 MT) + overpull (2 MT) and diverter came free. RB same in set back area and secured." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.5 hours. Operational details: Attached slings to chackles in bails in TDS to overshot joint. Removed tension bolts using Bandak Bolt Tensioning Tool. LO overshot joint and removed slings." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Held tool-box meeting. RIH and MU up flange connection to tensioner joint using 19 studs on B-type flange. Meanwhile installed riser spider and function tested same." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 6.0 hours. Operational details: Held tool-box meeting. Reduced pressure on tensioner cylinders in 20 bar steps from 150 MT to 55 MT (weight of LPDR when ran was 42 MT). Picked up 60 MT + block weight with TDS (reading 130 MT). Bled off all pressure on tensioner cylinders, leaving all riser tension in TDS. Dismantled tensioner system." "On 2007-07-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW to disconnect and POOH with LPDR." "On 2007-07-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WOW to disconnect and POOH with LPDR. Meanwhile prepared equipment for LO 6 3/4' DC. LD 1 std 6 3/4' DC in singles." "On 2007-07-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: WOW to disconnect and POOH with LPDR. Meanwhile LO 6 3/4' DC." "On 2007-07-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Re-installed riser trolly and cradle onto HTS. RD remainder of tensioner system prior to pulling LPDR. Held pre-job meeting prior to pulling LPDR." "On 2007-07-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Used rig tongs and turned LPDR 1/2 turn to the right to release RL-4 connection, release torque 50 kNm. Observed disconnect with ROV. PU clear of conductor and lifted LPDR up to rig floor slowly until first flange was above spider dogs. String WT 45 MT. Engaged spider dogs and inserted stop bolts. Landed LPDR." "On 2007-07-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 10.0 hours. Operational details: BO and LD 3 LPDR joints in singles (tension joint, upper pup joint and splash zone joint), using 5 1/2' elevator attached to handling flange B." "On 2007-07-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 6.0 hours. Operational details: BO and LD 3 LPDR standard joints in singles using 5 1/2' elevator attached to handling flange A." "On 2007-07-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 6.5 hours. Operational details: BO and LD 3 LPDR standard joints in singles using 5 1/2' elevator attached to handling flange A." "On 2007-07-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.5 hours. Operational details: RD LPDR handling equipment and cleared rig floor. Removed spider and excess equipment from rig floor. Removed equipment from wellhead area. Greased and serviced PRS's and TDS." "On 2007-07-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Held tool-box meeting prior to RIH with 3 1/2' DP. Rigged up for running 3 1/2' DP." "On 2007-07-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Trouble-shooted and repaired PRS software failure." "On 2007-07-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1350m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: MU cement stinger to 3 1/2' DP and RIH. Stabbed into conductor housing assisted by ROV. When RIH with 338 m of 3 1/2' DP, crossed over to 5 1/2' and continued RIH with cement stinger." "On 2007-07-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1350m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed side entry sub and single. Installed Lo-torque valve on side entry sub." "On 2007-07-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1352m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PU stand and connected to TDS. Tagged bottom at 1353.5 m (1.5 m fill). PU 1 m to 1352 m. Displaced hole to seawater, 1500 lpm/32-67 bar pumping 100 m3 SW. Lined up to kill mud." "On 2007-07-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1352m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Flow checked well and observed for bubles at wellhead with ROV. Rotated string with 5 rpm and reciprocated slowly. Meanwhile tested cement lines to 200 bar/5 min and held cement tool-box meeting with new crew. No gas observed." "On 2007-07-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1074m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Cemented plug #1 from 1352 m to 1079 m RKB: Mixed and pumped, 800 lpm/30 bar, 12,0 m3 1.90 SG 'G' cement slurry and displaced with 8.5 m3 seawater using rig pumps, 1500 lpm/ 3 bar, 50 rpm/1-2 kNm. POOH to 1074 m and dropped sponge ball and circulated 1.2 m3 hole volume with seawater, 2200 lpm/55 bar. PU to 1073 m." "On 2007-07-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 795m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Cemented plug #2 from 1073 m to 800 m RKB: Mixed and pumped, 800 lpm/27 bar, 12,0 m3 1.90 SG 'G' cement slurry and displaced with 5.5 m3 seawater using rig pumps, 1500 lpm/ 3 bar, 50 rpm/1-2 kNm. POOH to 795 m and dropped sponge ball and circulated 1.2 m3 hole volume with seawater, 2200 lpm/55 bar. PU to 794 m." "On 2007-07-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 251m. The activity was categorized as 'drilling -- wait' and lasted for 14.0 hours. Operational details: POOH with cement stinger to shoe at 251 m due to upcoming other activity on rig: Waited on Siemens software downloading for process module due to by-passed ESD systems." "On 2007-07-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 335m. The activity was categorized as 'drilling -- wait' and lasted for 1.0 hours. Operational details: MU and RIH with 3 1/2' cement stinger. Had a few tight spots, observed with ROV." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 795m. The activity was categorized as 'drilling -- wait' and lasted for 1.5 hours. Operational details: Crossed over to 5 1/2' DP and continued MU and RIH with cement stinger. Installed side-entry sub with Lo-torque valve." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 795m. The activity was categorized as 'drilling -- wait' and lasted for 0.5 hours. Operational details: Pumped btms up to clean well. Meanwhile held pre-job meeting with crew before cement job." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 516m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Cemented plug #3 from 794 m to 521 m RKB: Mixed and pumped, 800 lpm/26 bar, 12,0 m3 1.90 SG 'G' cement slurry and displaced with 2.5 m3 seawater using rig pumps, 1500 lpm/ 1 bar, 50 rpm/1-2 kNm. POOH to 516 m, dropped sponge ball and circulated 1.2 m3 hole volume with seawater, 2200 lpm/45 bar. PU to 515 m." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 374m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cemented plug #4 from 515 m to 249 m RKB: Mixed and pumped, 800 lpm/21 bar, 16,6 m3 1.95 SG neat 'G' cement slurry and displaced with 0.5 m3 seawater using cement unit, 1000 lpm/ 27 bar. POOH to 374 m." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Continued POOH w/ cmt stinger from 374m to 249 m. Dropped 2 sponge balls and circulated 1.2 m3 hole volume with seawater, 2200 lpm/45 bar. POOH" "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Laid out cmt assembly." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.8 hours. Operational details: Changed out wash pipe and tested same to 275 bars. Meanwhile ROV repaired damage on 30' housing." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Held tool box meeting prior to Slip and Cut Drill line" "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: Slip and Cut drill line." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Moved CTS funnel from F-4 to F-12, and installed hose." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Held tool box meeting prior to pick up 26' BHA and R/U for making up 26' BHA." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Picked up 26' Bit and motor assy. RIH same." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 3.0 hours. Operational details: Terminated operation due to Siemens uploading of Software" "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Helicopter operation, no crane available. Meanwhile greased TDS and Dolly." "On 2007-07-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Continued M/U 26' BHA. Had to use Rig tongs to M/U 17 1/4' stabilizer. Performed tool box meeting prior to M/U 17 1/4' stabilizer." "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Cont. M/U 26' BHA and RIH same. ROV monitored BHA entering funnel. RIH to one std above expected top cmt plug" "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 280m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Held tool box meeting with all invovled personel. Started RIH with 40 rpm and 3660 lpm. Tagged cmt at 257 m. Continued drilling from 257m to 280m 40 rpm, 3660lpm and 2 - 4 MT WOB." "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 335m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 26' hole from 280m to 335 m. 50 ROP, 40 rpm, 3660 lpm 2 -4 MT WOB. Pumped 30m³ 1.4 SG Pill 1990 lpm, 72 bars SPP, 40 rpm, 1-3 KNm TQ." "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 225m. The activity was categorized as 'drilling -- wait' and lasted for 3.8 hours. Operational details: Pulled out of hole to 225m. Stand-by due to prioity of Siemens to upgrads software. Meanwhile perform check of TDS for loose items." "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 376m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 26' hole from 335m to 376 m.40 ROP, 40 rpm, 3660 lpm, 88 bars SPP, 2 -4 MT WOB. Taking survay as required. Slide F/ 335 - 364 Slide F/ 370 - 376" "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 376m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Racked back one std due to ROV failure. Meanwhile circ at reduced rate 2013 lpm, 21.4 bars SPP. Inspected TDS. Terminated operation. Due to one double 3 ½' DP came out of derrick single latch and leaned over the windwall across the drill floor. Meanwhile continued repairing ROV." "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 370m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Investigated incident with 3 1/2' DP. Meanwhile circulated and reciprocate pipe, 3000 lpm 54,5 bars SPP, up/down weight 110/108 MT." "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 370m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Stopped rig pumps. Connected CTS hose to ROV and started same." "On 2007-07-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 431m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 26' hole from 376 m to 431 m. 40 rpm, 3660 lpm, 88 bars SPP, 2 -4 MT WOB. Taking survay as required. Sweep 15 m³ Hi-vis pill 3 times every std." "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 457m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 26' hole from 431 m to 457m sliding building angle. 3000 lpm, 2 - 6 MT WOB" "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 476m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 26' hole from 457 m to 476 m rotating 40 rpm, 4500 lpm, 149 bars SPP, 2 - 6 MT WOB, 4-5 kNm. Sweep 15 m³ Hi-vis pill 3 times every std." "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 497m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 26' hole from 476 m to 497m sliding. 4500 lpm. 2 - 6 MT WOB" "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 512m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 26' hole from 497 m to 512 m rotating. 40 rpm, 3500 lpm. 6 - 8 MT WOB 28 m/h. Sweep 15 m³ Hi-vis pill 3 times every std." "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 536m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 26' hole from 521 m to 536 m sliding. 4500 lpm. 8 MT WOB. 28 m/h" "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 880m. The activity was categorized as 'drilling -- drill' and lasted for 15.0 hours. Operational details: Drilled 26' hole from 536 m to 880 m . Parameters: 3670 - 5000 lpm, 88 - 178 bar SPP, 40 - 70 rpm, 4,3 KNm, 8 - 12 MT WOB, 30 - 53 m/hr ROP, 1,07 - 1,11 ECD. Pumped sweep 2 - 3 times every std 15m³. Held time-out for safety with night crew at 19:00." "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 880m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated well clean prior to enter Utsira, two times bottoms up, 5010 lpm, 172 bars SPP, pumped two hi-vis pills each of 15 m³, one at the start one in the middle." "On 2007-07-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 901m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Resumed drilling 26' hole. from 880 to 901 m Parameters: 3335 - 5000 lpm, 92 - 183 bar SPP, 40 - 70 rpm, 2 - 5 KNm, 11 - 21 MT WOB, 11 - 150 m/hr ROP, 1,06 - 1,08 ECD. Pumped sweep 2 - 3 times every std 15m³ Entered Utsira at 887 m." "On 2007-07-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1054m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Continued drilling 26' hole. from 901 to 1054 m Parameters: 2982 - 3338 lpm, 78 - 101 bar SPP, 70 rpm, 4,4 - 6,5 KNm, 2,8 - 10 MT WOB, 95 - 140 m/hr ROP, 1,06 - 1,20 ECD. Pumped sweep 2 - 3 times every std 15m³" "On 2007-07-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1054m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: At 1054 m attempted to rotate string after sliding. Picked up, circulated well clean 3338 lpm 98 bars. Started to rotate string and reciprocated slowly while circulating well clean." "On 2007-07-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 26' hole. from 1054 to 1082 m Parameters: 3338 lpm, 95 - 106 bar SPP, 0,0 - 6,3 KNm, 10 - 11 MT WOB, 12 - 172 m/hr ROP, 1,12 - 1,13 ECD. Pumped sweep 2 - 3 times every std 15m³" "On 2007-07-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- drill' and lasted for 15.0 hours. Operational details: Drilled 26' hole from 1081 m MD RKB to 1362 m MD RKB. Parameters: 4008 - 5350 lpm, 131 - 216 bar SPP, 40 - 70 rpm, 2 - 15,3 KNm, 2 - 12 MT WOB, 18 - 55 m/hr ROP, 1,07 - 1,11 ECD. Pumped sweep 2 - 3 times every std 15m³." "On 2007-07-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pumped 40 m³ Hi-vis and commenced circ. well clean. Meanwhile evaluated GR/Res log to confirm TD. Unable to identify base Skade on the GR/Res log, due to sensors still above base Skade." "On 2007-07-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Resumed drilling of 26' hole from 1362m MD RKB to 1369 m MD RKB. Parameters: 5010 lpm, 186 bar SPP, 2,3 KNm, 8,5 MT WOB, 17 m/hr ROP, 1,08 ECD." "On 2007-07-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Awaited GR/Res logs to be evaluated by duty Geologist. Meanwhile circulated well at 5478 lpm 213 bars. Continued as planned. TD confirmed to be at 1369m MD RKB." "On 2007-07-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.8 hours. Operational details: Pumped 40 m³ Hi-vis followed by 30 m³ sea water 40 m³ Hi-vis and circulated well clean with maximum rate 5477 lpm 213 bars (min. 3 x BU). Rotated string w/ 80 rpm and reciprocate. ECD 1,07. Held Tool box meeting prior to start pumping 1.35 SG mud." "On 2007-07-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Started to displace open hole to 1,35 sg mud. 3200 - 5010 lpm 79 - 236 bars. Rotated string with 20 rpm." "On 2007-07-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Completed displace well to 1.35 SG mud. Total pumped 480 m³." "On 2007-07-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 9.2 hours. Operational details: Attempted to POOH w/ BHA, tightspot F/ 1348m T/ 1330m. Worked string/backreamed 260 - 440 lpm, 1.35 SG mud, 5 - 8 bars, 13 -37 KNm, 50- 70 rpm, max overpull 20 MT." "On 2007-07-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 8.2 hours. Operational details: RIH to TD, circulated hole clean with SW 4500 lpm 165 bar, 80 rpm, 8 - 12 KNm. One mud pump out of services." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued circulate hole clean with SW 4500 lpm 165 bar, 80 rpm, 8 - 12 KNm. Mud pump #3 out of services." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1262m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Mud pump #3 up running. Increased rate to 5478 lpm, 224 bars, 80 rpm, started to ream out of hole 1 std/hr, 22 - 28 KNm, Hook load 145 MT, no overpull. At 1324m stopped rotation, no overpull. Pumped out of hole to 1313 m took OP of 20 MT, started to rotate 80 rpm. Continued ream out of hole 1 std/hr F/ 1220 m T/ 1262 m, 5478 lpm, 222 - 226 bars, 80 rpm, 8 - 28 KNm, Hook load 140 - 145 MT." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1220m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Racked back second std. Continued POOH T/ 1220 m, pumped 40 m³ of hi-vis, and displaced same OOH with SW, 5478 lpm, 217 bars, 80 rpm, 8 - 10 KNm, Hook load 140 - 145 MT, no overpull" "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1095m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH w/ 144 MT hook load F/ 1220m T/1095 12min/std. Pumped 40 m³ Hi-vis." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1095m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Circulated Hi-vis out of hole w/ SW at 5010 lpm, 180 bars." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1093m. The activity was categorized as 'drilling -- drill' and lasted for 6.2 hours. Operational details: POOH to 994 m, took over pull of 15 MT. Ran back in hole, met obstruction at 1093m, worked string, 333 - 5000 lpm, 3 - 179 bars, 5 - 15 rpm, 6 - 9 KNm. Lined up tool face high side, pumped 5000 lpm 179 bars, passed obstruction at 1093m. RIH F/ 1093m T/ 1101m." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1101m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Pumped 10 m³ Hi-vis followed by 1.5 btms up w/ SW, 5000 lpm, 179 bars, 50 rpm, 5 - 8 KNm." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1142m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH took weight at 1102 m rotated string, 330 lpm, 1 bar, 10 rpm, 13 - 15 KNm. Lined up tool face high side, 5000 lpm, 179 bars, passed obstruction. RIH F/ 1102m T/ 1142 m." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1142m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Pumped 10 m³ Hi-vis and circulated out same 5000 lpm, 179 bars. Rotated & reciprocated pipe F/1142 m T/ 1100m." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: RIH F/ 1142 m T/ 1369 m. Worked string, rotating/sliding high side. 3076 - 5010 lpm 82 - 190 bars, 0 - 20 rpm, 0.5 - 20 KNm." "On 2007-07-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Pumped 30 m³ Hi-vis, one btms up w/ SW, 25 m³ Hi-vis, 1.5 btms up w/ SW. 5500 lpm, 226 bars. 80 rpm. Rotated & reciprocated pipe F/ 1369m T/ 1355m." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued circulate out 1.5 btms up w/ SW. 5500 lpm, 226 bars. 80 rpm. Rotated & reciprocated pipe F /1369m T/ 1355m." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Displaced 200 m³ 1.4 SG mud. 5478 lpm, 259 bars. 80 rpm. Rotated & reciprocated pipe F/ 1369m T/ 1355m." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1002m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: POOH w/ 26' BHA. F/ 1369m T/ 1002m. Lubricated out due to over pull of 20 MT. F/ 1340m T/ 1303m and F/1102m T/1002. 442 lpm, 2.5 bars, 80 rpm, 8 - 20 KNm." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 870m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH w/ 26' BHA. Lubricated F/ 1002m T/ 870m. 442 lpm, 2.5 bars, 80 rpm, 8 - 20 KNm." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 870m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Displaced hole to 200 m³ 1.40 SG mud above Utsira. 4500 lpm, 165 bars, 80 rpm, 3 - 7 KNm." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 415m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Continued POOH F/ 870m T/ 415 m. Reamed back F/ 525 m T/ 415 m. 442 lpm, 2.5 bars, 80 rpm, 5 - 10 KNm." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 415m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Displaced well to surface with 140 m³ 1.40 SG mud. 4500 lpm, 168 bars, 80 rpm, 0 - 5 KNm." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued POOH F/ 415 m T/ 120 m. ROV observed well when pulling out of 30' housing." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Held tool box meeting, racked back BHA in derrick. Stabilizers covered with clay." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Cleaned Rig Floor. Simultaneously transfered CTS funnel from F-12 to F-4." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box meeting prior to lower DCI frame from rig floor to below cellar deck." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Removed protector guides on tensioner and centralizer deck. Lowered CTI frame to scaffolding below cellar deck and secured same." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed PDM head to 20', Cleared rig floor." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to RU for CSG running." "On 2007-07-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: R/U for running 20' CSG. Changed bails, elevators." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Continued R/U for running 20' CSG. Installed FAC tool, R/U CSG tong, dressed PS-30 slips, installed protector guides on tensioner and centralizer deck." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued rigging up for running 20' casing." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Troubleshoot problem w/casing tong" "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held pre-job meeting prior to run 20' CSG." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Pick up 20' shoe, intermediate and float, and thread locked same." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed CSG guide on Odfjell spider elevator due to ID being 9mm to small." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 20' CSG F/12m T/36m" "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting, re-installed modified CSG guide to elevators." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continued RIH F/36m T/52M" "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PRS not operational - ET calibrated PRS." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Continued RIH w/20' casing F/52m T/151m. Filled every joint w/sw. Had ROV to guide 20' CSG shoe into 30' conductor, continued running 20' casing to 214m." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Replaced two sheared bolts to the make up and break out function on the piston latch of the 20' CSG tong." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued RIH F/ 214m T/ 249m. Engaged FAC tool into 20' casing and pumped 27m³ 1.4 SG mud, 1667 lpm, 27 bars." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box meeting with night shift for running 20' CSG. Released FAC tool." "On 2007-07-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 460m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RIH with 20' CSG. F/249m T/460m. Filled every jnt with rest of 20m³ 1.40 SG mud, continued with SW. Had tight spot at 419m set down 6 MT, Engaged FAC tool and lubricated through obstruction at 419m." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 812m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Continued RIH with 20' CSG. F/460m T/812m." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 838m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued RIH w/ 20' CSG F/812m T/838m" "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 838m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Due to incorrect torque, broke CSG jnt out and inspected threads. Meanwhile held tool box meeting with day shift." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1045m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Continued RIH w/ 20' CSG F/838m T/1045m. Tight spot F/923m T/937m, set off 7 - 10 MT and washed through. Started investigating problems with casing tong load sensor." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1045m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Unable to make up CSG properly, investigated CSG tong, found fault in load censor and in software. Laid out two jnt w/ overtorqued threads, Replaced same w/ jnts from deck" "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued RIH w/ 20' CSG F/1045m T/1083m" "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1095m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: At 1083m met obstruction. Worked casing down w/ 1200 - 200 lpm and 5 - 50 MT to 1095m." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1120m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Continued to wash CSG down F/1095m T/1106m. Hit obstruction at 1106m washed down from 1106m to 1120m." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1203m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH w/ 20' CSG F/ 1120m T/1203m." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1203m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Removed 20' CSG automatic slips and installed manuel 20' CSG slips. Modified automatic slips to 5½' DP slips. Removed 20' CSG elevator, bails and FAC tool. Installed bails and 5½' DP elevator." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1203m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to pick up and run in w/ 18 3/4' Subsea well head." "On 2007-07-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1203m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up 18 3/4' Subsea well head, attempted to make up same, had problems getting 18 3/4' Subsea well head vertical without the possibility of damaging the threads." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1203m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out 18 3/4' Subsea well head and inspected threads. Postioned 18 3/4' Subsea well head vertical and made up same." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1203m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Orientated DCI inlet on 18 3/4' Subsea well head, within 90º - 45º to port side pointing east." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1222m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Removed RT bushing ran 18 3/4' Subsea well head below RT. Installed bushing and 5½' slips. Landed 18 3/4' Subsea well head." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1222m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: R/D 20' CSG tong. Re-established Iron roughneck." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1222m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to run in with the 18 3/4' Subsea well head on 5½' HWDP." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1246m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Ran in with 20' CSG and 18 3/4' Subsea well head. Positioned DCI inlet on 18 3/4' Subsea well head below celler deck." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1246m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to make up DCI frame on to 18 3/4' Subsea well head." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1246m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Started to attach DCI frame on to 18 3/4' Subsea well head." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1246m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Attached DCI frame to 18 3/4' Subsea well head, had to re-align DCI inlet. Installed check sub." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1246m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up CSG string 0.5m weigth 250 MT. Pressure tested DCI frame on 18 3/4' Subsea well head to 3000 psi as per Vetco procedure." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1246m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Re-orientated DCI frame on 18 3/4' Subsea well head." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1246m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Dismantled scaffolding below cellar deck, to be able to run DCI frame through." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1262m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up 2 jnt HWDP from cantilever and RIH with landing string." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1262m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Problem with HTS software. Investigated same" "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1324m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH w/ landing string F/1262m T/1324m. Took up/down weight 230/190 MT prior to land 18 3/4' Subsea well head." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1324m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Orientated DCI frame on 18 3/4' Subsea well head using the ROV." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Landed off 18 3/4' Subsea well head and took 25 MT overpull. Kept 3 MT overpull on landing string." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk prior to pick up cmt head. Picked up cmt head and made up same." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk prior to pick up and make up cmt hose. Picked up cmt hose and made up same." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk prior to perform cmt job. Simultaneously established circulation w/ SW picked up rate in steps F/1340 lpm T/2300 lpm." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Mixed and performed cmt job. Pumped : 238.5 m³ 1.56 SG lead slurry at 900 - 1100 lpm, 25 - 35 bars pump pressure. 20 m³ 1.92 SG tail slurry at 800 - 1000 lpm, 20 - 30 bars pump pressure." "On 2007-07-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Released dart, chased dart with SW at 3000 lpm, FCP 56 bars. At 9370 stks bumped plug increased pressure to 96 bars. 96,7 % pump efficiency." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Bled off pressure and checked for backflow to Halliburton cement unit, 1.2 m³ bled back. Bled off pressure in landing string." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to R/D cmt hose. R/D same cmt hose and control lines for operating the cmt head." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set down 2 MT on CART and marked DP on drill floor. Turned string 5 right hand turn and released CART. Pulled 1.5m above 18 3/4' Subsea well head." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Washed 18 3/4' Subsea well head area with SW at 5000 lpm, using the landing string as washing tool. Inspected 18 3/4' Subsea well head, found both pad eyes visible." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk prior to L/D cmt head, L/D cmt head." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Dropped two Halliburton sponge balls and flush string using seawater at maximum rate." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Pull out of water w/ landing string and CART. Measured landing string." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Continued L/O landing string. Held tool box talk with day shift prior to L/O CART. L/O 18 3/4' CART. B/O subs from FAC tool and L/O same." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleared rig floor and excess equipment in preparation for L/O 26' BHA." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Held tool box talk prior to L/O 26' BHA. L/O 26' bit and MWD power puls. Broke dog collar links." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Replaced broken dog collar links." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Continued L/O remaining 26' BHA." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared and tidied rig floor prior to run HPDR." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: R/U for HPDR, placed tension ring around F-12 on centralizer deck, rigged up and tested hydraulic spider, installed riser supports to HTS, installed guide lines in moonpool for HPDR and removed hatches on top level of platform." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held a detailed pre-job safety meeting, regarding picking up and running of the HPDR." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Built scaffolding barriers around all open well bay areas on each working level on the platform." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk with night shift prior to run HPDR." "On 2007-07-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Prepared and picked up Tie Back Connector and stress jnt. Made up Tie Back Connector and stress jnt." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Made up Fairing (anti collision protection) and run with HPDR to next flange connection. Made up third connection of HPDR." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Function tested Tie Back Connector" "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Attached guide wire clamp above Tie Back Connector." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Continued run in with HPDR. Held tool box talk with day shift prior to pick up HPDR double 'B'. Picked up and made up same. ROV latched on both guide wires to template." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Waited on crane, due to helicopter crew change." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Picked up and ran in with HPDR 'B'. Simultaneously prepared tools and equipment for installation of centralizers, tension ring and cylinders." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Made up tension jnt and fairings." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk prior to pick up BOP jnt with Claxton tool installed. Picked up BOP jnt with Claxton tool and parked in 5½' elevators." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Buildt scaffolding in Moon pool to get access for installation of BOP." "On 2007-07-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Made up BOP jnt with Claxton tool." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Held tool box talk prior to remove Spider slips and installation of master bushing. Commenced removal of Spider slips and installed master bushing" "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked one 5½' DP stds and made up same to Claxton tool.. Simultaneously laid out Spider slips from rig floor." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed 18 3/4' Subsea well head protection cover and verified BX ring to be in correct position." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Ran to ½ m above 18 3/4' Subsea well head, came down 10 cm at the time to just above the VX seal ring. Attempted to land TBC, when TBC was pushed aside due to current, VX ring came off." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: ROV came to surface and picked up new VX ring. Installed the new VX ring on wellhead." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Ran in with TBC and HPDR to +/- 5 cm above VX ring to much movement of the TBC to be able to land off on to 18 3/4' Subsea well head. Secured riser in Moon Pool area to see if any change in movement." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Awaited for TBC to be stable prior to land same." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box talk prior to move guide wires to slots F-4 & F-6. Prepared and moved guide wires to slots F-4 & F-6, to assist in stabbing the TBC. Meanwhile cleared aft set back area to be ready for picking up 5½' DP." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Stabbed TBC and released centralizing slings in Moon pool area. Commenced to land riser as per Vetco procedure, set down 20 MT." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Launched Vetco hot stab and ran same to TBC. Latch on with ROV and locked H4-MUSL connector as per Vetco procedure. Pressured up in stages to 206 bars. Meanwihile picked up 5½' DP from pipe deck." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Applied 10 MT overpull on riser to confirm H4-MUSL connector. Filled riser with SW. Lost overpull due to filling up w/ SW and adjusted for same. Completed filling up riser with SW. Measured distance from RBK to Bottom of Claxton tool to 10.925 m." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed 1502 Veco blind plug on Claxton tool and lined up to cmt unit to pump through TDS. Performed integrity test of the 20' casing and riser to 20/195 bars 5/10 mins. Bled down in stages." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held pre-job meeting prior to installing centralisers, tension ring and cylinders. Meanwhile retrieved hot stab on TBC and replaced with dummy. Retrieved guide wires from template." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Installed centralisers and boat collison stool." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Installed tension ring and cylinders. Applied tension of 80 MT to the cylinders." "On 2007-07-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to disconnect Claxton tool" "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Disconnected Claxton tool. Racked back one 5½' DP std and removed Claxton tool from rig floor. Cleared and cleaned rig floor area. (Crew change at 01:00)" "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to nipple up BOP." "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Modified scaffolding around NT2 connector. Moved BOP tension cylinders and erected scaffolding around BOP test stump." "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.5 hours. Operational details: Erected scaffolding around BOP test stump. Commenced transporting of BOP carrier over NT2 riser connector. Cleaned BOP seal face and installed new seal ring. Centralized and secured HPDR. Landed the BOP and made up BOP clamp to 1600 ft/lbs. Meanwhile picked up 5½' DP from pipe deck." "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.5 hours. Operational details: Installed BOP tensioners, installed diverter and measured for slick jnt." "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk prior rig up for testing TDS. Rigged up same." "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Held tool box talk prior to test lines. Flushed lines. Commenced pressure testing of the TDS to 30/345 bars 5/10 mins. Worked valves several times to get a good test." "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Rigged down test assy and hoses." "On 2007-07-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk prior to pick up test plug." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up bull nose jetting sub, test plug and RIH same." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Unable to RIH due 19' diverter insert still installed. Removed same." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 142m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Ran in with test plug and jet sub from surface to 135m. Washed down to 142m at 1700 lpm and 75 rpm." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Ran in and landed off test plug in well head." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk prior to pressure test of the BOP NT2 connection and HPDR. Commenced pressure test 25/345 bars 5/10 min. Started to pull out of hole when hydraulic hose bursted on the iron roughneck rollers." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Repaired hydraulic hose and fitting." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH with test plug and jet sub assy." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Broke and laid down BOP test plug and jet sub." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to running nominal seat protector." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up WBRT/nominal seat protector and RIH on 5 1/2' DP." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Malfunction on AFT PRS. investigated situation, found bursted hose in dragchain." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Brought work basket to drillfloor. Prepared permit and repaired hose in dragchain." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Tested AFT PRS after repair. Found hose in dragchain to be thight but otherwise ok. Decided to use FWD PRS to continue RIH with WBRT/nominal seat protector." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Continued to RIH with WBRT/nominal seat protector on 5 1/2' DP." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Set nominal seat protector according to Vetco procedure at 141,3 m MD. Set down 5 MT, pull tested with 3 MT overpull." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: POOH with WBRT, broke out and laid down same." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing diverter." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Picked up diverter and set aside. Thightened slick-joint/overshot connection on the BOP. Filled riser with water and verifed connection holding hydrostatic pressure. Installed diverter in housing." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Clear and tidied rigfloor. Held toolbox talk prior to making up 17 1/2' drilling BHA." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Made up 17 1/2' drilling BHA to ADN sub." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Fenced of drillfloor and WH module prior to handling RA source. Transferred RA source from shipment container to installation carrier. Attempted to install RA source in ADN - nogo." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: Made several attempts to install the RA source in the ADN sub - nogo. Attempted with dummy RA source - ok." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 50m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.2 hours. Operational details: Discussed situation, suspected thread damage on RA source. Decided to change to backup ADN and RA source. Moved RA source from installation carrier to shipment container, thread mated correctly inside shipment container. Reconsidered action and made new attempt to install RA source. Removed adapter on ADN and transferred source directly from the installation carrier into the ADN. Installed RA source succesfully." "On 2007-07-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued to make up 17 1/2' drilling BHA. Made up NM drillcollar." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 320m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Continued to make up 17 1/2' drilling BHA. Made up 8 1/4' drillcollar, jar/accelerator, x-over and 5 1/2' HWDP. Installed PS-30 slips." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP. Picked up and made up 27 singles." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued RIH with 17 1/2' drilling BHA on 5 1/2' DP stands." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1100m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued RIH with 17 1/2' drilling BHA on 5 1/2' DP to 1100 m MD." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1100m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Connected TDS for test of MWD/LWD tools. Encountered problems with mudpumps #1 and #3 when bringing up the rate." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1100m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Leakage observed on mudpump #1. Liner spray on mudpump #3 not working. Repaired mudpumps." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1100m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed test of MWD/LWD tools. Brought pump rate up to 3500 lpm / 101 bar SPP. Not able to establish communication with ARC tool." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1260m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued to RIH with 17 1/2' drilling BHA from 1100 m to 1260 m MD. Picked up single to space out for drilling shoetrack on 1 stand." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1288m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Brought pumprate to 3000 lpm and washed down from 1260 m to 1288 m MD. Dumphose not handling flow => routed return flow to shakers and pumproom." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1319m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued washing down from 1288 m to 1319 m MD at 3000 lpm. Tagged obstruction at 1319 m MD with 5 MT WOB." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1319m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Attempted to Perform choke drill. Rig choke sensors not reading pressures." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1319m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Investigated sensor fault. Found faulty I/O module and sensor. Prepared for reparing sensor." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1319m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Brougth pumps up to 4500 lpm and observed/rearranged dumphose to take full return flow. Meanwhile worked on choke sensors." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1319m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Continued repairing choke sensors. Meanwhile cleaned and tidied in Moonpool, shaker area and BOP control room." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1319m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed choke drill." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1326m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Established drilling parameters 3000 lpm / 50 RPM and reamed section from 1319 m to 1326 m MD. Tagged firm cement at 1326 m MD." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1330m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled firm cement from 1326 m MD to 1330 m MD. Drilling parameters : Flow 4000-4500 lpm / SPP 130-160 bar / 80-90 rpm / 3-10 MT WOB / Torque 10-20 kNm - string stalled out on occasions. Reamed as required. Drilled float collar at 1330 m MD." "On 2007-07-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled cement in shoetrack from 1330 m to 1355 m MD. Drilling parameters 4000 lpm / SPP 130 bar / 90 rpm / 3-5 MT WOB / Torque 16 kNm." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling cement in shoetrack from 1355 m to 1358 m MD. Drilling parameters 4000 lpm / SPP 130 bar / 90 rpm / 3-5 MT WOB / Torque 16 kNm." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Drilled cement in rathole from 1358 m to 1367,5 m MD. Drilling parameters 4000 lpm / SPP 131 bar / 50-80 rpm / 3 MT WOB / Torque 15 kNm. Reamed back to shoe for every 2 m drilled. Reamed through shoe without rotation last time - no obstructions. Performed toolbox talk prior to displacement." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Displaced well to 1,35 sg Performadrill KCl mud. Pumped 25 m3 hi-vis followed by 30 m3 of drillwater and 220 m3 1,35 sg Performadrill. Pump rate 2000-4000 lpm / SPP 80-190 bar / rotation 20 rpm. Closed dumpline valve and routed interface mud to pit#12." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Routed mud returns to pit#7 and circulated on closed system. Picked up single 5 1/2' DP for drilling rathole." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1372m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled from 1367,5 m to 1372 m MD with reduced ROP due to problems with cold mud overflowing the shakers." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1372m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Criculated and conditioned mud at reduced rate 2200 lpm due to overflowing on shakers." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pulled back into 20' casing without pumping." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Circulated and conditioned mud with bit inside 20' casing. Changed shaker screens to 145 mesh. Established flowrate of 4500 lpm." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Lined up cement unit down standpipe and kill line. Flushed lines with mud prior to XLOT. Closed BOP on 5 1/2' DP." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Performed XLOT. Pressured up 1st cycle at 100 lpm. Did not achieve expected response." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Verified line up by closing in and releasing 10 bar down drillstring and kill line - ok." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Continued XLOT. Pumped 1000 liter at 100 lpm to get to 8-10 bar, zeroed counter. Pumped an additional 500 liter to 26 bar. Unexpected respons. Bled back pressure." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: Pressured up again with same volume at 200 lpm. Monitored trip tank for leakage above BOP - none detected. Repeated cycle twice more up to approx 50 bar at 100/200 lpm. No definitive leak off pressure could be determined. Prepared for work on standpipe valves." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Dismanteled manual choke valve on standpipe manifold. Greased valve S2, 10 and 11." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Pressure tested standpipe manifold. Valves S3, 6, 7, 8 and 11 tested ok." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Lined up pumps and flowline for drilling. Stepped up rate to 4500 lpm. Cycled flowrates 3800/4500 lpm to set Powerdrive according to instructions from DD. Fast procedure failed. Reverted to long procedure, Powerdrive set - ok." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1422m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 17 1/2' section from 1372 m to 1422 m MD. Inserted and drilled with 1 singel to complete tally. Drilling parameters : Flow 4500 lpm / SPP 235 bar / 120 rpm / 10 MT WOB / Torque 15-20 kNm." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1422m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Started setting Powerdrive for corrections needed according to directional plan. Cycled rate 3800/4500 lpm. Had overload of cuttings conveyer belt which was shut down by safety switch. Had to stop pumping because the cuttings conveyer belt had stopped." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1422m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Worked to clean and re-start cuttings conveyer belt." "On 2007-07-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1431m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued cycling rate at 3800/4500 lpm to set Powerdrive. Continued drilling from 1422 m to 1431 m MD." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1436m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 17 1/2' section from 1431 m to 1436 m MD. Had to stop drilling due to prevailing problems with cuttings conveyer belt. Not able to restart belt." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1436m. The activity was categorized as 'interruption -- other' and lasted for 4.8 hours. Operational details: Conveyer belt could not be restarted as the shute in which the belt is running was full of cuttings. Opened forward shute on conveyer system to bring cuttings forward into skip. Emptied conveyer screws in shaker room into skips. Removed cuttings from conveyer belt shute with HP guns, fire hoses and suction hoses. Cleaned up cuttings from deck. Meanwhile circulated well with low rate and rotated string at 20 rpm." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1461m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 17 1/2' section from 1436 m to 1461 m MD. Drilling prameters : Flow 4500 lpm / SPP 238 bar / 130 rpm / 2-3 MT WOB / ECD 1,37 sg / Torque 16 kNm. Restricted ROP to 30 m/hrs to check capacity of cuttings transport on conveyer belt." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1476m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 17 1/2' hole from 1461 to 1476 m MD. Drilling parameters : Flow 4500 lpm / SPP 239 bar / 150 rpm / 5-10 MT WOB / Torque 18 kNm. ECD: 1,375 SG" "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1476m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Took survey and downlinked Powerdrive by cycling rate 3800/4500 lpm. Observed blockage on cuttings conveyer screw in shaker room." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1476m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Took SCR and calibrated MWD depth. Meanwhile worked to open blockage in cuttings convery screw." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1476m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Worked to open blockage/remove cuttings from conveyer screws in shaker room." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1476m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Made connection and synchronized Powerdrive." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1476m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 17 1/2' section from 1476 m to 1512 m MD. ECD: 1,375 SG" "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1512m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Cycled pumprate 3800/4500 lpm to downlink Powerdrive. Blockage on cuttings conveyer screw in shaker room." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1512m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Worked to open blockage/remove cuttings from conveyer screws in shaker room." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1512m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Made connection and took MWD survey." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1546m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued drilling 17 1/2' section from 1512 m to 1546 m MD. Cuttings conveyer belt on main deck stopped moving/packed with cuttings." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1546m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Attempted to unplug/clean conveyer belt - nogo. Decided to pull into casing shoe while making repairs and modifications to the conveyer belt system." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1467m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' drilling BHA from 1546 m to 1467 m MD. Tight hole took approx 30 MT overpull." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1354m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Continued POOH with 17 1/2' drilling BHA while pumping from 1467 m to 1354 m MD inside casing." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1354m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Lined up well on triptank. Changed from PS-30 to manual slips. Static losses approx 100 l/hrs." "On 2007-07-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1354m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Made modifications to cuttings conveyer belt : -Cut and fitted drainage hatch -Prepared IBC underneath drain -Fit bracket for flushing with fire hoses -Narrowed orifice of discharge shute Meanwhile serviced top drive. Tested path for cuttings transport and fluid discharge through the DCI system - ok. Static losses 30 l/hrs." "On 2007-07-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1354m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Continued making modifications to cuttings conveyer belt." "On 2007-07-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1541m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: RIH with 17 1/2' drilling BHA from 1354 m to 1541 m MD. Pumped at 2000 lpm on way in / no rotation. Took weight and reamed through ledges at 1390 m MD and 1396 m MD. Meanwhile continued modifications on cuttings conveyer belt." "On 2007-07-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1541m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Tagged fill at 1541 m MD. Stepped up rate to 4500 lpm. Worked to get stable conditions on shakers and cuttings conveyer belt. Took cuttings partly to conveyer belt and partly to DCI unit with overboard discharge. Cut back rate to 3500 lpm to get stable condtions on shakers." "On 2007-07-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1546m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Washed from 1541 m to 1546 m MD. Parameters : Flow 3500 lpm / SPP 162 bar / 120 rpm / <1 MT WOB / Torque 13 kNm." "On 2007-07-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1859m. The activity was categorized as 'drilling -- drill' and lasted for 17.0 hours. Operational details: Drilled 17 1/2' hole section from 1546 m to 1859 m MD. Driling parameters : Flow 4500 lpm / SPP 248 bar / 180 rpm / 3-5 MT WOB / Torque 14-23 kNm / ECD 1,37-1,38. Took surveys on connections. Reamed stand before connections. Downlinked Powerdrive at 10:15. Experienced problems with Mudpump #2." "On 2007-07-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1859m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Mud pump #1 down failed, washout in valve seat, shut down pump. Mud pump #1 also out of service. Had to stop drilling. Reciprocated on stand while working on mud pump #2." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1859m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Continued working on mud pump# 1 and 2. Meanwhile : -Reciprocated on stand pumping 1800 lpm / rotation 30 rpm -Attempted to make up 14' casing joints in doubles, inserts and guides on PRS to tight for 14' casing" "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1809m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Continued working on mud pump # 1 and #2. Attempted to remove suction valve seat - nogo. Removed the complete suction valve seat housing and replaced with housing from mud pump #1. Meanwhile set back one stand and reciprocated on previous stand." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1859m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH with 17 1/2' drillng BHA for recommencement of drilling." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1881m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 17 1/2' section from 1859 m to 1881 m MD. Driling parameters : Flow 4500 lpm / SPP 250 bar / 180 rpm / 6 MT WOB/ Torque 20 kNm / ECD 1,38. Performed SCR." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1959m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 17 1/2' hole section from 1881 m to 1959 m MD. Drilling parametes : Flow 4500 lpm / SPP 250 bar / 180 rpm / 3-4 MT WOB / 22 kNm / ECD 1,37-1,38. Found bent/loose die retainer plate on TDS." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1940m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Had to change die retainer plate on TDS. Circulated hole clean. Installed manual slips. Racked back 1 stand and installed side entry circulation sub. Hooked up coflex for circulation while working on TDS." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1940m. The activity was categorized as 'interruption -- other' and lasted for 3.8 hours. Operational details: Dismanteled and replaced die retainer plate on TDS. Meanwhile circulated at 1500 lpm." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1940m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Tested torque wrench on TDS - ok. Installed automatic slips." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1972m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued drilling 17 1/2' hole from 1959 m to 1972 m MD. Drilling parameters : Flow 4500 lpm / SPP 255 bar / 180 rpm / 3-4 MT WOB / 22 kNm / ECD 1,37-1,38." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1972m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Shakers overflowing due to new mud being circulated. Cut back on flowrate and worked string until satisfactory flowrate of 4500 lpm could be achieved." "On 2007-07-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2080m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 17 1/2' hole from 1959 m to 2080 m MD. Drilling parameters : Flow 4500 lpm / SPP 246 bar / 180 rpm / 3-4 MT WOB / 21 kNm / ECD 1,37-1,38. Performed survey and reamed stand on connection. Downlinked Powerdrive as required. Meanwhile ROV attached DCI hose to subsea clumpweights - ok." "On 2007-07-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2146m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 17 1/2' hole section from 2080 m to 2146 m MD. Drilling parameters : Flow 4500 lpm / SPP 258 bar / 180 rpm / 3-4 MT WOB / 23 kNm / ECD 1,37-1,38. Downlinked Powerdrive as required. Performed pit drill at 02:00. Bled 2-3 m3 mud into active. Good response from driller and Geoservice. Experienced problems with mud pumps, standpipe pressure eratic and lower than before." "On 2007-07-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2150m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot problems with mudpumps, isolated one pump at the time. Problem with mud pump #2, took pump out of service. Attempted to drill ahead using mud pump #1 and #3. Got problem with mud pump #1." "On 2007-07-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2150m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Stopped drilling. Worked on mud pump #2, changed ejection valve and valve seat. Meanwhile reciprocated string pumping 1500 lpm with mud pump #3. Rotated string 20 rpm." "On 2007-07-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2320m. The activity was categorized as 'drilling -- drill' and lasted for 10.5 hours. Operational details: Continued drilling from 2150 to 2320 m MD. Drilling parameters : Flow 4500 lpm / SPP 265 bar / 180 rpm / 10-12 MT WOB / Torque 20-25 kNm / ECD 1,37-1,38. Performed survey and reamed stand on connection. Downlinked Power as required." "On 2007-07-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2403m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: Drilled 17 1/2' hole section from 2320 to 2403 m MD. ROP dropped to 5-10 m/hrs, increased WOB. Drilling parameters : Flow 4500 lpm / SPP 265-272 bar / 180 rpm / 10-18 MT WOB / Torque 16-23 kNm / ECD 1,37-1,38. Top of Balder encounterd at 2345 m MD. Stick slip tendencies at 2380 m MD, reduced WOB as required." "On 2007-07-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2417m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 17 1/2' hole section 2403 m to 2417 m MD. Drilling parameters : Flow 4500 lpm / SPP 275 bar / 180 rpm / 18 MT WOB / Torque 20 kNm / ECD 1,37-1,38. ROP down to 4-6 m/hrs." "On 2007-07-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2417m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Due to decreasing ROP, picked 0,3 m off bottom to clean the bit. Increased pump rate to 4700 lpm and rotated at 220 rpm and held for 10 mins. Got problems with mud pump #3, took pump out of service, reciprocated on stand pumping 2000 lpm. Lined up mud pump #2. RIH and stepped up pumps to 4500 lpm for commencement of drilling." "On 2007-07-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2438m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued drilling 17 1/2' hole section from 2417 m to 2438 m MD. Drilling parameters : Flow 4500 lpm / SPP 276 bar / 180 rpm / 15-18 MT WOB / Torque 24-30 kNm / ECD 1,37-1,38. ROP increased to appox 10 m/hrs. Drilling break at 2431with ROP of 20 m/hrs. Experienced stick slip tendencies at 2436 m MD, decreased WOB as required." "On 2007-07-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2486m. The activity was categorized as 'drilling -- drill' and lasted for 8.5 hours. Operational details: Continued drilling 17 1/2' section from 2438 m to 2486 m MD. Drilling paramaters : Flow 4500 lpm / SPP 272-280 bar / 150-180 rpm / 13-15 MT WOB / Torque 17-24 kNm / ECD 1,37. Took survey and reamed singel on connection. Got problems with mud pumps #2 and #3." "On 2007-07-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2486m. The activity was categorized as 'interruption -- other' and lasted for 7.2 hours. Operational details: Worked on mud pumps #2 and #3. Changed swab/piston and liner seal on pump #2. Changed liner spray hose on pump #3. Got pump #2 up and running. Attempted to recommence drilling at 21:45. Observed leakage on TDS washpipe." "On 2007-07-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2444m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Had leakage on TDS washpipe. Installed manual slips. Installed side entry circulation sub. Connected cement hose and circulated 1300 lpm while working on washpipe. Parked topdrive and changed washpipe." "On 2007-07-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2444m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Continued changing washpipe on TDS. Greased TDS." "On 2007-07-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2486m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Finished working on TDS. Installed automatic slips. Made up stand and RIH to 2486 m MD, stepped up pumps and recommenced drilling." "On 2007-07-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Continued drilling 17 1/2' section from 2486 m to 2505 m MD. Drilling paramaters : Flow 4500 lpm / SPP 280-284 bar / 180 rpm / 8-12 MT WOB / Torque 19-25 kNm / ECD 1,37. ROP dropped from 10 m/hrs to 2 m/hrs towards 2505." "On 2007-07-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2513m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled 17 1/2' section from 2505 m to 2513 m MD. Drilling parameters : Flow 4500 lpm / SPP 280-284 bar / 180 rpm / 8-12 MT WOB / Torque 19-25 kNm / ECD 1,37. ROP dropped from 2 m/hrs to 1 m/hrs towards 2513. Decided to pull out of hole to change bit." "On 2007-07-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2513m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Circulated hole clean with 4500 lpm / SPP 285 bar while reciprocating on stand." "On 2007-07-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2254m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 17 1/2' drilling BHA from 2513 m to 2254 m MD." "On 2007-07-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1798m. The activity was categorized as 'drilling -- trip' and lasted for 7.0 hours. Operational details: Tight hole from 2254. Continued POOH while pumping at 3500 lpm from 2254 to 1798 m MD. Rotated at 40 rpm on 15 MT+ overpull as dictated by hole." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1661m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Continued POOH with 17 1/2' BHA from 1798 m to 1661 m MD pumping at 3500 lpm. Rotated at 40 rpm on 15 MT+ overpull as dicated by hole." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1661m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Due to pack off tendencies at 1661 m MD, increasing ECD > 1,40 and increasing cuttings trend over shakers => Reciprocated and circulated on stand at 4500 lpm / 20 rpm. Decreased ECD from 1,402 to 1,390 with continuous flow of cuttings over shakers." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1523m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued to POOH with 17 1/2' drilling BHA from 1661 m to 1523 m MD. Sticky conditions. Pumped at 3500 lpm / Rotation 40 rpm. ECD 1,39-1,40." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1439m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' drilling BHA from 1523 to 1439 m MD. Sticky conditions. Increased flow rate when pulling to 4500 lpm due to increasing ECD > 1,40. Rotated at 40 rpm." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1337m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 1439 to 1337 m MD. Sticky conditions. Increased flow rate when pulling to 4500 lpm due to increasing ECD > 1,40. Rotated at 40 rpm." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1337m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Circulated hole clean. Pumped at 4500 lpm. Rotation 30-40 rpm." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1337m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked prior to POOH in 20' casing - well static. Pumped 4 m3 slug of 1,55 sg mud." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1337m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 17 1/2' drillling BHA on 5 1/2' DP from 1337m to 1335 m MD. Tight hole at 1335 m MD when stabilizer entering shoetrack. Unable to pull without swabbing." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1035m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Made up TDS to pipe and continued pulling from 1337 m to 1035 m MD while pumping at 1300-3000 lpm. Rotated as dictated by hole 10-40 rpm. At 1115 m MD increased flowrate to 4000 lpm." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 1035 m to 800 m MD. No tight spots observed. Pumped 2 m3 slug of 1,55 sg mud." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 266m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 800 m to 266 m MD. Flowchecked prior to POOH with 17 1/2' BHA - well static." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 163m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' HWDP from 266 m to 163 m MD." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 163m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Held toolbox talk. Removed automatic slip and installed master bushing." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Continued to POOH with 17 1/2' BHA. Racked back drillcollars and jar/intensifier." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: With ADN sub in rotary, prepared for handling/removing RA source. Rigged up adapter and transfer shield. Fenced off drilling area. Attempted to remove RA source from ADN - nogo." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Troubleshot situation. RA source seemed to unscrew but was still hanging on threads. No back up transfer shield onboard in case shear pin release. Decided to try to pull RA source with the possible implication that back up ADN tool could not be run." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Pulled RA source using tugger. Source came free, threads seemed to be OK. Transferred RA source to transport container. Planned for picking up backup ADN and backup RA source." "On 2007-07-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Picked up 17 1/2' drilling BHA and lifted above rotary. Inspected bit. Prepared for breaking bit." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Broke out 17 1/2' PDC bit using bit breaker and manual tongs. Made up new 17 1/2' rock bit to Powerdrive. Torqued bit to 37000 ft lbs using manual tongs. Gauged bit, checked nozzles and rollers." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 9m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Broke out an laid down ADN, Sonic and ARC tools. RIH with Powerdrive and hung off same in rotary. Cleared drillfloor and prepared for service on TDS." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 9m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Worked on TDS. Checked TDS for noise while rotating. Changed gear oil on TDS." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Made up and RIH with backup ARC, backup Sonic and Powerpulse." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Made up ADN to 17 1/2' drilling BHA." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Held toolbox talk. Connected TDS and tested MWD tool pumping at 3000 lpm / SPP 50 bar - ok." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Held toolbox talk. Transferred and installed RA source in ADN tool using tranfer shield and transfer rod. Had problems to function fingers on collar fingerboard." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Troubleshot fingerboard communication with AD control panel." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 205m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: RIH with 17 1/2' drilling BHA from 40 m to 205 m MD on 5 1/2' HWDP to locate RA source below sealevel." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 205m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Continued to work on collar fingerboard." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH with 17 1/2' drilling BHA from 205 m to 40 m MD on 5 1/2' HWDP." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to operating collar fingers manually." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RIH with 17 1/2' drilling BHA on DC and 5 1/2' HWDP from 40 m to 200 m MD." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed master bushing. Installed automatic slips." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1031m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP/HWDP from 200 m to 1031 m MD. Had problems with fingerboard. Meanwhile performed well control drill." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1031m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot fingerboard." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1345m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Continued to RIH with 17 1/2' drilling BHA on 5 1/2' DP from 1031 m to 1345 m MD." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1345m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Filled drillpipe and broke circulation in shoetrack. Pumped at 3000 lpm / SPP 135 bar." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1415m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued to RIH with 17 1/2' drilling BHA on 5 1/2' DP from 1345 m to 1415 m MD. Reamed thightspots at 1360, 1362 and 1378 m MD with 4500 lpm / 80 RPM." "On 2007-07-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2238m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2 DP from 1345 m to 2238 m MD - hole condition good." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2238m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Connected TDS, filled pipe and broke circulation." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2470m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued to RIH with 17 1/2' drilling BHA on 5 1/2' DP from 2238 m to 2470 m MD. Hit obstruction at 2470 m MD." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2482m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Brought pump up to 4300 lpm / SPP 293 bar and reamed with 120 rpm to clear restriction. Still took some weight on bit. Reduced rate an downlinked Powerdrive according to instructions from DD. Reamed down to 2482 with 0-2 MT WOB while setting Powerdrive." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2513m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Made connection. Performed SCR. Performed MWD survey. Reamed down to 2513 with 4300 lpm and 120 rpm." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2524m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 17 1/2' hole from 2513 m to 2523,5 m MD. Drilling parameters : Flow 4360 lpm / SPP 284-296 bar / 180 rpm / 12-19 MT WOB / Torque 23 kNm / ECD 1,391-1,394. ROP 5-7 m/hrs. Trip gas peaked at 12000 ppm." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2524m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Performed survey. Circulated hole clean => Reciprocated on stand, increased pumprate to 4500 lpm / 293 bar SPP / rotation 120 rpm. ECD when starting 1,393. ECD at 06.00 1,389. MW out 1,37. Started to add Graphite and Calcarb to active." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2524m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued to circulate hole clean with 4500 lpm." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2524m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Made connection. Performed MWD survey. Stepped up pumps to drilling rate at 4500 lpm." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2535m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drilling 17 1/2' hole from 2523,5 m to 2535 m MD. Drilling parameters : Flow 4500 lpm / SPP 282 bar / 180 rpm / 20 MT WOB / Torque 24 kNm / ECD 1,38. ROP 5 m/hrs. Failure on mud pump #1 and mud pump #3." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2535m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Worked on mud pumps #1 and #3. Changed discharge valve and seat on MP#3. Changed suction valve, seat and cap seal on MP#1. Meanwhile reciprocated and circulated at 1500 lpm / 50 rpm." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2541m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued drilling 17 1/2' hole from 2535 m to 2541 m MD. Drilling parameters : Flow 4500 lpm / SPP 282 bar / 180 rpm / 12 MT WOB / Torque 24 kNm / ECD 1,38. ROP 5 m/hrs." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2541m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Checked for losses - ok." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2548m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drilling 17 1/2' hole from 2541 m to 2548 m MD. Drilling parameters : Flow 4500 lpm / SPP 282 bar / 180 rpm / 20 MT WOB / Torque 24 kNm / ECD 1,38. ROP 12 m/hrs" "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2548m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Checked for losses - ok." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2569m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: Continued drilling 17 1/2' hole from 2548 m to 2569 m MD. Drilling parameters : Flow 4500 lpm / SPP 272-280 bar / 180 rpm / 12-18 MT WOB / Torque 24 kNm / ECD 1,37. ROP 1-2 m/hrs. Had drilling break at 2569 m MD, ROP increased to 10 m/hrs over 0,8 m drilled, then decreased again. Dynamic losses of 1-2 m3/hrs. Encountered erratic data on incl. azim. sensor on powerdrive." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2572m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 17 1/2' hole from 2569 to 2572,5 m MD. Drilling parameters : Flow 4500 lpm / SPP 282 bar / 180 rpm / 12 MT WOB / Torque 24 kNm / ECD 1,37. ROP 1-2 m/hrs. Log response indicating top of Ty penetrated. Dynamic losses approx 3 m3/hrs. Lost connection with PowerDrive sensors, incl, az, GR." "On 2007-07-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2572m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Circulated bottoms up at 4500 lpm to obtain bottom sample." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2572m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Circulated bottoms up at 4500 lpm to obtain bottom sample. Dynamic losses 1,8 m3/hrs." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2572m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Obtained sample and verified section TD at 2572,5 m MD, 19 m MD into Ty formation." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2529m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Lined up pumps to pump Calcarb/Graphite LCM pill down drillstring. Pumped 19 m3 LCM pill at 2000 lpm while rotating 30 rpm. Spotted pill from 2572,5 m MD to 2567 m MD. Broke connection and spotted pill from 2567 m to 2529 m MD. Checked for losses - no static losses." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2529m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Cirulated well clean. Stepped up pumps to 4500 lpm and reciprocated on stand with 120/180 rpm rotation. Reset Powerdrive according to instructions from DD. Dynamic losses 0,5 m3/hrs." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2490m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Broke connection set back stand and continued to clean well on next stand. Circulated at 4500 lpm with 120/180 rpm rotation while reciprocating string." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2528m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Circulate hole clean at 4500 lpm and 120/180 rpm rotation while reciprocating on stand." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2528m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well - well static." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 2528 m to 1357 m MD: Pulled wet pipe. Minor tightspots (max 10 MT overpull) observed at : 2254, 2252, 2120, 1924, 1939, 1652, 1535 m MD. Intervall 1520 m to 1480 m MD, max 18 MT overpull. Intervall 1385 m to 1357 m MD, max 18 MT overpull. No rotation and/or circulation needed." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well inside casing shoe - well static. Pumped 10 m3 of 1,55 sg slug for pulling dry pipe." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 830m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 1357 m to 830 m MD. Got problems with iron roughneck." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 830m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Repaired bursted hydraulic hose in iron roughneck dragchain" "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued to POOH with 17 1/2' drilling BHA on 5 1/2' DP/HWDP from 830 m to 200 m MD." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well prior to pulling 17 1/2' BHA - well static. Removed automatic slips and installed masterbushing." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Pulled 17 1/2' drilling BHA from 200 m to 63 m MD. Racked back drillcollars, jar and intensifier." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Rigged up adapter and transfer shield on top of ADN tool. Removed RA from ADN source and transferred same to transportation container." "On 2007-07-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Broke out and laid down ADN, Sonic and ARC logging tools. Laid down Powerdrive." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleared and tidied rigfloor." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Made up cement stand with pups and singel. Not able to rack back because cement head was to heavy causing buckling of 5 1/2' DP. Broke out and laid down pipe again. Left 4,5 m pup on cement head." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Made up WBRRT tool and jet sub on 5 1/2' HWDP. RIH and located pipe accross BOP. Operated rams. Jetted/washed BOP with 2000 lpm." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with WBRRT tool. Measured out pipe and washed accross nominal seat protector twice with 3000 lpm. Latched on to nominal seat protector at 140,12 m MD and released same with 15 MT overpull." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Dropped 2 15/16' drift. POOH with WBRRT/nominal seat protector on 5 1/2' HWDP. Retrieved drift and laid down WBRRT tool." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Rig up for running 14' casing. Installed casing tong on iron roughneck and hooked up hydralics. Hooked up FAC tool to TDS. Changed links and elevator." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: 14' air operated elevator needed dual air inlet, but only one available from TDS. Produced and hooked up hose tee on elevator air supply." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Attempted to pick up and make up cement head to 5 1/2' pup joint and singel in mouse hole and rack back in collar finger - nogo. Stand was bending and it could not be set back as the PRS needed to change grip for racking. Broke out singel and laid down cement head and singel." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held prejob meeting prior to running 14' casing. Meanwhile finished hooking up 14' casing running equipment." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: P/U shoe joint and hung off in rotary." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Took time out as adviced by Statoil drilling supervisor. Emphasized that everyone working regulary on the drillfloor should use proper radio gear." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Picked up and made up 14' intermediate joint and float collar joint. Threadlocked couplings. Used manual slips when handling. Tested shoe and float collar joint for flowthrough and flowback - ok." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 68m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up and made up double 14' casing. Threadlocked coupling. Made up 5 m 14' casing pup joint. Filled casing." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 68m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Installed Odfjell flush mounted slips in rotary. Tested slips for potential casing lift out, casing lifted out. Adjusted opening pressure of slips, reattempted lift out - ok." "On 2007-08-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 236m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Ran 14' casing according to tally from 68 m to 236 m MD. Filled every joint while running. Average running speed 3-4 jnts/hr." "On 2007-08-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 390m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Ran 14' casing according to tally from 236 m to 390 m MD. Filled every joint while running. Average running speed 5 jnts/hr." "On 2007-08-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 580m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Ran 14' casing according to tally from 390 m to 580 m MD. Filled every joint while running. Average running speed 5-6 jnts/hr." "On 2007-08-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 11.0 hours. Operational details: Ran 14' casing according to tally from 580 m to 1357 MD. Filled every joint while running. Average running speed 6 jnts/hr." "On 2007-08-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated at 20' shoe at 1357 m. Pumped 220 lpm and broke circulation at 48 bar. Increased pump rate to max 1500 lpm. No losses. Meanwhile serviced casing running equipment and cleared floor of protectors. Up weight 221 MT/ down weight 201 MT." "On 2007-08-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1609m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Ran 14' casing according to tally from 1357 to 1609 MD. Filled every joint while running. Average running speed 5-6 jnts/hr." "On 2007-08-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1609m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Checked Flush Mounted Spider (FMS) for loose/broken items due to cracking sound when MU casing joint. Nothing was found." "On 2007-08-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1752m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Ran 14' casing according to tally from 1609 to 1752 m MD. Filled every joint while running. Average running speed 6-7 jnts/hr." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2182m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Ran 14' casing according to tally from 1752 to 2182 MD. Filled every joint while running. Average running speed 6-7 jnts/hr." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Ran 14' casing according to tally from 2182 m to 2422 m MD. Filled every joint while running. Average running speed 7 jnts/hr." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Remove FMC slips and installed master bushing/manual slips. RD FAC tool and 500 MT elevator. RU rig bails and elevator." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PU and MU 14' casing hanger. RIH and jammed casing coupling in inner bushings in rotary table." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Trouble-shooted casing coupling jamming. Removed inner bushing and master bushing. Ran casing hanger through rotary. Installed bushings and sat slips." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2427m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed casing tong and stored on set back area." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2512m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran 14' casing according to tally from 2427 m to 2512 m MD. Took max 40 MT weight at 2512 m. MU TDS, broke circulation and attempted to pass restriction. No go. Started to circulate at 220 lpm, 12 bar and increased flow to 470 lpm, 14.3 bar. Broke free upwards with 400 MT/down 296 MT." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2513m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Washed 14' casing down from 2512 m to 2513 m MD, 550 lpm, 16 bar, 20-25 MT down weight." "On 2007-08-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2514m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Continued to work through tight spot and washed 14' casing down from 2513 m to 2513.5 m MD, 1000-1400 lpm, 18-40 bar, 25-35 MT down weight. Max allowed pressure was 55 bar." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2514m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Continued to work through tight spot and washed 14' casing down from 2513.5 m to 2514.5 m MD, 1400-2000 lpm, 20-40 bar, 20-45 MT down weight. Max allowed pressure was 55 bar. Observed loss at 2000 lpm." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2515m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Continued to work on tight spot at 2515 m MD, 200-2000 lpm/ max 60 bar and max 70 MT down weight. Free upweight 430-470 MT." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2402m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pumped out of hole, 200 lpm, and RB 3 stds HWDP. Free upweight ~430-470 MT in Lista Fm. Above Lista Fm, free upweight 410-420 MT." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2402m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RU casing tong. BO 14' casing hanger and LD same." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2402m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held tool box meeting prior to RU and LO casing. Changed bails and elevators. RU air lines to TDS." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2357m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH and LD 5 joints of 14' csg from 2422 m to 2357 m MD." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2357m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Changed bails and elevator. RD air lines to TDS." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: PU 14' csg hanger assembly. Removed csg tong. Washed down 3 stds and 2 singles HWDP from 2366 m to 2496 m MD, 500 lpm, 7 bar. PU and MU cmt head. RIH and landed off 14' csg hanger. 14' land-off point @ 140.32 m MD. Top 14' @ 140.0 m." "On 2007-08-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated one csg volume of 1.35 sg WBM using rig pumps, 2300 lpm and 36 bar. Meanwhile RU cmt hoses and held tool box meeting prior to cmt job. Decreased flow to 2190 lpm and 35 bar loss free rate." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued circulating one csg volume of 1.35 sg WBM using rig pumps, 2190 lpm and 35 bar." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pumped 21 m3 1.63 m3 sg Tuned Spacer using rig pumps, 1500 lpm and 17 bar. Dropped ball for bottom plug. Mixed and pumped 31 m3 1.90 sg cmt slurry, 800 lpm 25-34 bar. BTM plug sheared at approx 50 bar. Pumped 890 liter WBM to displace cement to rig floor. Released dart. Displaced wiper plug by pumping 3 m3 WBM with cement unit, 1200 lpm and 45 bar. Top plug sheared at 207 bar/977 ltr." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Displaced cement with rig pumps, 2440 lpm and 6.5 bar Increased displacement rate to 3000 lpm when cement entered annulus. Slowed down rate to 1200 lpm approx 3 m3 prior to bump. Recorded FCP 32 bar. Bumped plug with 187.7 m3 (8559 strokes) and pressured up to 103 bar. Bled back 870 ltr to cement unit and checked for back flow. Disconnected cement hose." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Sat seal assembly according to Vetco procedure by releasing over-pull and setting down 7-8 MT. Rotated landing string 4-41/2' turns right-hand. Started pressure testing surface lines to 207 bar." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continue to set seal assembly according to Vetco procedure. Bled off pressure and opened upper rams. PU to 30 MT overpull and closed rams." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Tested MS seal assembly, 35 bar/345 bar 5min/15 min using cement unit. Volume pumped, 436 ltr." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Reduced from 30 MT to 3 MT overpull. Rotated 4 turns to the right to release running tool. PU PADPRT and landing string. Removed lo-torque before RB cmt stand (2 x HWDP and cmt head)." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2505m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Dropped 2 x sponge balls into HWDP. MU TDS and pumped 1.35 sg WBM at 3350 lpm, 29 bar." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH and LO PADPRT. Measured lead impression block. Cleared and cleaned rig floor." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: MU jet sub, WB RT and wear bushing. RIH to 140 m. Installed wearbushing and POOH. Meanwhile RU gyro unit on rig floor." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Tested gyro downhole tools on rig floor. Meanwhile performed maintenace on TDS and PM's and house keeping." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2470m. The activity was categorized as 'workover -- wire line' and lasted for 5.0 hours. Operational details: RIH with gyro from RKB to 2470 m MD. Performed gyro survey while POOH." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: LD tools and tested same. RD gyro unit and cleared rig floor." "On 2007-08-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: LO jet sub and wear bushing RT assembly. LO cement head assembly." "On 2007-08-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continue LO cement head assembly." "On 2007-08-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Held tool box meeting prior to rigging up to pull diverter. Removed elevators and RU to pull diverter. Pulled diverter to rig floor. RU 'C' spanner to bell nipple and undid nut. Removed seals and cleaned area. Found upper seal to be damaged. Meanwhile installed check valve and DCI hose on wellhead using ROV. Broke ROV handle on DCI hose." "On 2007-08-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 13.0 hours. Operational details: Continued to work on leak in BOP slick joint. MU BOP mandrel to BOP. PU and ran diverter. Connected hydraulic hoses and overshot hose. Installed outer ring and master bushing. RD diverter handling equipment. Meanwhile RU slurry filter pump, performed maintenace and house keeping and prepared equipment for testing BOP." "On 2007-08-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: Filled hole with 1.35 sg WBM and tested overshot seals. Closed shear ram and tested 14' csg and shear ram 30/345 bar 5/15 min with cement unit. Pumped and bled back 3 m3. Meanwhile RD diverter handling equipment and RU 5 1/2' DP handling equipment." "On 2007-08-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: MU and RIH with bull nose jetting tool and jetted BOP and wearbushing. Circulated 4000 lpm and 90 bar. Meanwhile located lead 'plug' in kill line and removed same." "On 2007-08-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Picked up BOP test tool and space out assembly." "On 2007-08-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: RIH with BOP test tool and landed off." "On 2007-08-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.0 hours. Operational details: Pressure tested BOP according to Mærsk procedure. Meanwhile changed out hose on PRS and continued housekeeping." "On 2007-08-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Continued pressure testing BOP according to Mærsk procedure. Meanwhile changed out hose on PRS and continued housekeeping." "On 2007-08-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: RU chicksan and manifold for testing TDS and kelly hose. Flushed and tested TDS and kelly hose 35/345 bar 5/10 min. POOH with BOP test assembly. LO pup-joint, DP and test plug. Cleared and cleaned rig floor. Meanwhile changed out hose on PRS and continued housekeeping." "On 2007-08-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 12.0 hours. Operational details: Cleaned moonpool, BOP, all levels in wellhead and future equipment room. Meanwhile performed initial start-up of CRI and injection on 14' x 20' annulus. Formation fractured at 71 bar. Injection pressure leveled out at 110 bar with 1000 lpm seawater. Shut down pumps and pressure leveled out at 37.5 bar." "On 2007-08-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 9m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk and started MU and RIH with 12 1/4' BHA." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 324m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: MU and RIH with 12 1/4' BHA from 9 to 324 m MD. Handled radioactive sources and installed 6 5/8' Totco ring below 5 1/2' HWDP. Weight below jar is 16 MT." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: MU and RIH with 12 1/4' BHA from 324 m to 1000 m MD." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: MU TDS and tested downhole tools at 3500 lpm, 153 bar." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1327m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: MU and RIH with 12 1/4' BHA from 1000 m to 1327 m MD." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1327m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Found trip tank displacement to be equal to metal displacement and not the calculated 646 l/std. Closed annular and pumped through lower kill to see if float was holding. Observed immediate pressure increase on DP side." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1327m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held tool box talk prior to POOH and change float. RU mud bucket." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: POOH with 12 1/4' BHA from 1327 m to 200 m MD to change float. Pumped slug when BHA at surface." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Removed auto slips and installed master bushings and inserts." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: POOH with 12 1/4' BHA from 200 m to surface. Removed radioactive source from ADN at 47 m." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Held tool box talk with new crew. Broke off 12 1/4' bit and LO powerdrive. PU and MU 12 1/4' bit and backup powerdrive with pre-installed float. RIH with ADN to 26 m MD." "On 2007-08-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Inspected and evaluated damaged setting pistons on Stetho Scope. Decided to RIH with backup Stetho Scope." "On 2007-08-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: PU and MU backup Stetho Scope." "On 2007-08-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 486m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: MU and RIH with 12 1/4' BHA from 26 to 324 m MD. Programed sonic vision tool and loaded radioactive sources according to Schlumberger procedure. Weight below jar is 16 MT." "On 2007-08-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1410m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: MU and RIH with 12 1/4' BHA from 324 m to 1410 m MD. MU TDS and tested downhole tools at 3500 lpm, 148 bar at 1000 m." "On 2007-08-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1410m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Observed incorrect displacement while RIH. Pumped at high flow rate in an attempt to free any debris inside float. Lined up to pump down kill line with annular closed to test float. Pumped down kill line with 30 bar and observed communication into drill string." "On 2007-08-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: POOH with 12 1/4' BHA from 1410 m to 200 m MD." "On 2007-08-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Lined up to locate leakage in 12 1/4' BHA. Tested drill string through kill line and observed pressure drop. Continued to POOH and tested each std via kill line for possible wash out. Found leakage in energizer. LD energizer and BO MWD tools due to battery life." "On 2007-08-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: POOH with 12 1/4' BHA from 143 m to surface. LO jar and PU new jar. BO and LO MWD tools and downloaded radioactive sources. Unlatched battery on Stetho Scope." "On 2007-08-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Held tool box meeting. Performed cut and slip of drill line." "On 2007-08-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 69m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: MU and RIH with 12 1/4' BHA to 69 m MD." "On 2007-08-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1327m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: MU and RIH with 12 1/4' BHA from 69 m to 1327 m MD. Filled pipe every 10 stds. MU TDS and tested downhole tools at 3500 lpm, 168 bar at 1000 m." "On 2007-08-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2450m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: RIH with 12 1/4' BHA from 1327 m to 2450 m MD. Filled pipe every 10 stds." "On 2007-08-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2477m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Washed down from 2450 m and tagged cmt at 2477 m, 1000 lpm and 36 bar." "On 2007-08-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2478m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled on float equipment from 2477 m to 2478.5 m with 1.35 sg WBM. Worked with drilling parameters, 1750-2500 lpm, 60-122 bar, 0-120 rpm, 0-27 kNm, 1-10 MT WOB. Lifted off bottom systematically while drilling float equipment to engage in float and to allow flushing below bit." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled out shoe track and shoe with 1.35 sg WBM from previous section, 2490 lpm, 125 bar, 70 rpm, 16-29 kNm, 0-0.5 MT WOB. Started to see WOB (3-4 MT) from 2503.9 - 2505.9 m. Cleaned shoe track stepwise in 1-2 m steps. Spaced out with one single to have only one connection during cleaning of rate hole. Pulled through shoe track without rotation to verify no restrictions." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2520m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Cleaned out rathole from 2505.9 m to 2520 m with 1.35 sg WBM from previous section, 3340 lpm, 194-202 bar, 70 rpm, 25-29 kNm, 0.5-1 MT WOB, ECD 1.39. Cleaned rathole stepwise in 2-3 m steps. No bridge/ledge encountered when drilling out the section from 2512 to 2515 m where the casing couldn't pass." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2573m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Cleaned out rathole from 2520 m to 2573 m MD with 1.35 sg WBM from previous section, 3340 lpm, 200 bar, 70 rpm, 26-28 kNm, 0.5-1 MT WOB, ECD 1.39, ROP 20 m/hr. Up weight 195 MT/ down weight 160 MT." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2576m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled new formation from 2572.5 m to 2576 m MD, 3600 lpm, 225 bar, 100 rpm, 29-33 kNm, 6 MT WOB, ECD 1.39, ROP 6 m/hr." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2576m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated 1 1/2 btms up until shakers were clean. Mud weight stable at 1.38 sg." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2576m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RB 2 stds and one single to pull into 14' shoe. Held tool box talk prior to FIT. Verified correct line up and performed line test, 50 bar/5 min. Performed FIT to 1.48 sg EMW. Pumped up a MWD survey to confirm FIT to 1.486 sg EMW. Meanwhile built stds of 5 1/2' DP." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2576m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.2 hours. Operational details: RIH to bottom and observed no obstruction while RIH. Meanwhile held tool box meeting prior to displacement and confirmed line up. Displaced well to 1.35 sg OBM, 3600 lpm, 260 bar, 60 rpm, 22 kNm according to Baroids displacement plan. Filled sand traps and surface equipment with OBM and started to condition mud, 3340 lpm, 225 bar, 60 rpm. Up weight 180 MT/ down weight 145 MT. Meanwhile down linked MWD tools." "On 2007-08-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2576m. The activity was categorized as 'interruption -- repair' and lasted for 4.8 hours. Operational details: Trouble shot MWD transmission failure. Worked mud pumps at different rates and different configurations while rotated and resiprocated pipe. Bleed down and increased pressure on pulsation dampners, 300 psi/1100 psi. Closed one stand pipe. Managed to get good signal." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2576m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Continued to trouble shoot MWD transmision failure. Down linked tool to 3 bit signal density. Started with bit on bottom and reduced pump rate to keep tool in sync. Got good signal with valid drilling parameters." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 12 1/4' hole from 2576 m to 2616 m MD with 1.35 sg OBM, 3340 lpm, 200 bar, 180 rpm, 30 kNm, 2-3 MT WOB, ECD 1.365, ROP 20-25 m/hr. Down linked and performed survey as required. PU off bottom and observed well for losses at 2607 m. Well was static." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2616m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Lost signal from MWD tool on connection. Started with bit on bottom and reduced pump rate to keep tool in sync. Got good signal with valid drilling parameters." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2640m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 12 1/4' hole from 2616 m to 2640 m MD with 1.35 sg OBM, 3270 lpm, 189 bar, 180 rpm, 30 kNm, 2-3 MT WOB, ECD 1.37, ROP 20 m/hr. Down linked and performed survey as required." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2647m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 12 1/4' hole from 2640 m to 2647 m MD with 1.34 sg OBM, 3300 lpm, 202 bar, 180 rpm, 31-32 kNm, 0-1 MT WOB, ECD 1.37, ROP 5 m/hr. Down linked and performed survey as required." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2647m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Reamed from 2646 m to 2610 m while MWD had signal loss." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2740m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled 12 1/4' hole from 2647 m to 2740 m MD with 1.35 sg OBM, 3300-3500 lpm, 199-230 bar, 140-180 rpm, 28-44 kNm, 6-8 MT WOB, ECD 1.37, ROP 10-40 m/hr. Down linked and performed survey as required." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2740m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated hole clean at 3600 lpm, 230 bar, 180 rpm prior to taking pressure points. Reciprocated string. Specified where to take pressure samples with Statoil geologist." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2697m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: POOH and correlated into setting depth at 2697 m, 3425 lpm, 216 bar and no rotation. Down linked tool to 6 bit signal density. Took pressure reading with Stetho Scope at 2679,4 m according to Schlumberger instructions. Up weight 141 MT/down weight 142 MT. Pumped OOH after pressure reading from 2697 to 2640 m, 900 lpm, 21 bar, 90 rpm. Observed 10 MT overpull while POOH after pressure reading." "On 2007-08-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2619m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Had problems down linking to Stetho Scope. Made 3 attempts, recycled tool, down linked to sleep mode and back and worked with different flow rates before the tool took the command." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2638m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: POOH and correlated into setting depth at 2637.8 m and 2608.5 m. Took pressure readings with Stetho Scope at 2619.5 m and 2591 m according to Schlumberger instructions." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2740m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA to current TD. Down linked to MWD tools and set power drive." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2766m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 12 1/4' hole from 2740 m to 2766 m MD with 1.35 sg OBM, 3430-3565 lpm, 208-215 bar, 150 rpm, 22-40 kNm, 5-7 MT WOB, ECD 1.38, ROP 2-10 m/hr. Down linked and performed survey as required." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2771m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 12 1/4' hole from 2766 m to 2771 m MD with 1.35 sg OBM, 3390 lpm, 215 bar, 150 rpm, 22-40 kNm, 8 MT WOB, ECD 1.38, ROP 8 m/hr. Down linked and performed survey as required." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2771m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: RB one std and repaired damaged die carriers on TDS." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2811m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: Drilled 12 1/4' hole from 2771 m to 2811 m MD with 1.35 sg OBM, 3480-3560 lpm, 220-224 bar, 150-170 rpm, 18-45 kNm, 5-9 MT WOB, ECD 1.38, ROP 4-14 m/hr. Down linked and performed survey as required. Meanwhile built stds of 5' DP in derrick with forward PRS." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2811m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Had problem with PRS ZMS system. Circulated while rectifying problem." "On 2007-08-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2842m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 12 1/4' hole from 2811 m to 2842 m MD with 1.35 sg OBM, 3560 lpm, 220-224 bar, 150 rpm, 30-37 kNm, 7-10 MT WOB, ECD 1.38, ROP 2-14 m/hr. Down linked and performed survey as required. Meanwhile built stds of 5' DP in derrick with forward PRS." "On 2007-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2872m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole from 2842 m to 2872 m MD with 1.35 sg OBM, 3560 lpm, 220-224 bar, 150 rpm, 30-37 kNm, 7-10 MT WOB, ECD 1.38, ROP 2-9 m/hr. Down linked and performed survey as required. Meanwhile built stds of 5' DP in derrick with forward PRS." "On 2007-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2955m. The activity was categorized as 'drilling -- drill' and lasted for 13.8 hours. Operational details: Drilled 12 1/4' hole from 2872 m to 2955 m MD with 1.35 sg OBM, 3560 lpm, 230-235 bar, 150 rpm, 20-45 kNm, 8-9 MT WOB, ECD 1.38-1.39, ROP 5-9 m/hr. Down linked and performed survey as required. Meanwhile built stds of 5' DP in derrick with forward PRS." "On 2007-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2963m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: Trouble shot MWD transmission failure. Worked mud pumps at different rates and different configurations while rotated and resiprocated pipe. Down linked tool to 3 bit signal density. Started with bit on bottom and reduced pump rate to keep tool in sync. Got good signal with valid drilling parameters." "On 2007-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2964m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 12 1/4' hole from 2855 m to 2965 m MD with 1.35 sg OBM, 3430 lpm, 215 bar, 150 rpm, 20-45 kNm, 8-9 MT WOB, ECD 1.38-1.39, ROP 5-9 m/hr." "On 2007-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2965m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 12 1/4' hole from 2865 m to 2966 m MD with 1.35 sg OBM, 3430 lpm, 215 bar, 150 rpm, 20-45 kNm, 8-9 MT WOB, ECD 1.38-1.39, ROP 5-9 m/hr." "On 2007-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2966m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Had black-out in Geoservices unit due to flooding. Cleaned up water and restarted system." "On 2007-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2973m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled 12 1/4' hole from 2966 m to 2973 m MD with 1.35 sg OBM, 34300 lpm, 214-215 bar, 150 rpm, 25-36 kNm, 8-9 MT WOB, ECD 1.38-1.39, ROP 1-5 m/hr. Down linked and performed survey as required." "On 2007-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- drill' and lasted for 17.2 hours. Operational details: Drilled 12 1/4' hole from 2973 m to 3017 m MD, 3540 lpm, 223-239 bar, 140 rpm, 18-45 kNm, 7-10 MT WOB, ECD 1.38-1.40, ROP 1-4 m/hr. Increased mud weight to 1.40 sg OBM from 3000 m. Down linked and performed survey as required. Up weight 199 MT / Down weight 140 MT." "On 2007-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3017m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Wash pipe started leaking at 3017 m MD. Lined well up on trip tank. POOH to 3013 m and RB one std. Held tool box talk." "On 2007-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3017m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Monitored well while MU swedge, TIW and cement hose and established circulation at 30 spm, 20 bar. Changed and pressure tested wash pipe with mud pump to 250 bar. RD cement hose, TIW and swedge." "On 2007-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3030m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 12 1/4' hole from 3017 m to 3030 m MD with 1.40 sg OBM, 3540 lpm, 237-243 bar, 140 rpm, 10-45 kNm, 9-10 MT WOB, ECD 1.40-1.41, ROP 2-6 m/hr. Down linked and performed survey as required." "On 2007-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Continued drilling 12 1/4' hole from 3030 m to 3080 m MD with 1.40 sg OBM, 3540 lpm, 239-241 bar, 140 rpm, 10-45 kNm, 7-10 MT WOB, ECD 1.40-1.41, ROP 2-5 m/hr. Down linked and performed survey as required." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3110m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 12 1/4' hole from 3080 m to 3110 m MD with 1.40 sg OBM, 3540 lpm, 239-241 bar, 140 rpm, 10-45 kNm, 7-10 MT WOB, ECD 1.40-1.42, ROP 2-10 m/hr. Down linked and performed survey as required." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3114m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued drilling 12 1/4' hole from 3110 m to 3114 m MD, 10 meters past the Hot Shale. With 1.40 sg OBM, 3540 lpm, 239-241 bar, 140 rpm, 10-45 kNm, 7-10 MT WOB, ECD 1.41, ROP 2 m/hr. Down linked and performed survey as required." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Pulled of bottom and circulated with 3540 lpm, 160 rpm, 10-28 kNm, reciprocated string. Meanwhile added LCM materials. Continued circulating well clean, racked back one stand for every second BU. Took up/down weight 200/142 MT static 165 MT. Recorded touque at 10 rpm 20 kNm and 20 rpm 18 kNm." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2893m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH F/ 3113 m T/ 2893 wet. M/U TDS and pumped 5 m³ 1.6 SG slug and chased same with 4m³ OBM." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2506m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Continued POOH to 14' shoe F/ 2893m T/ 2506 m, max drag of 10 MT. Flow checked for 15 min while rotating with 10 rpm." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2405m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH F/ 2506m T/ 2405m liner hanger setting depth. M/U TDS, took up/down weight 177/143 MT and 159 MT static stretch 0.5 m. Recorded torque at 10 rpm 10-12 kNm and 20 rpm 10-13 kNm. Dropped 2 3/4' drift." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 234m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: Continued POOH F/ 2405m T/ 234m." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 234m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Flow checked well with BHA below BOP. Meanwhile inspected aft PRS dies and replaced same. Well static." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 234m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pulled PR-21 auto slips and installed master bushing, cleared rig floor." "On 2007-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Commenced to POOH with BHA and L/O same." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Continued L/O BHA, Held tool box talk prior to handing of Radio activ source. Unloaded radio activ source from tool." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: Continued L/O BHA to pipe deck." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Commenced dumping data from the Sonic tool. Cleaned rig floor." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Continued dumping data from Sonic tool. Meanwhile performed general maintenance." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting with all involved personal prior to run 9 5/8' liner." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: R/U liner handling equipment, removed master bushing, installed FMS, installed 9 5/8' inserts in BX elevators." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up shoe." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U shoe, intermediate, and landing collar, made up same with Bakerlock." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 9 5/8' liner filling every single F/ 38m T/ 122m." "On 2007-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: Continued RIH with 9 5/8' liner filling every 5th joint F/122m T/ 651m." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 698m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued RIH with 9 5/8' liner filling every 5th joint F/651m T/ 698m." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 698m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Removed FMS and installed master bushing." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 698m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up Liner Hanger." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 712m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up Liner Hanger and made up same, as per Weatherford procedure." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 712m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Rig down casing tong and hydraulic hoses. Cleared rig floor. Installed PS-21 slips." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued RIH with 9 5/8' Liner on 5½' DP F/712m T/1033m." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3069m. The activity was categorized as 'drilling -- casing' and lasted for 8.5 hours. Operational details: Continued RIH with 9 5/8' Liner on 5½' DP F/1033m T/3069m, filling every 5th std." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3115m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: M/U to TDS and washed down F/3069 m T/ 3115m @ 500 lpm, 10 bars. Tagged bottom at 3115m, took up/down weight 210/145 MT static 156 MT." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3115m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Racked back one stand. Made up cmt head and surface lines." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Commenced circulation of 1½ open hole volume, 1960 lpm @ 78 bar. Simultaneously held tool box talk prior to cmt job." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Dropped the ball and set the liner hanger according to Weatherford procedure. Liner hanger set at 2413m, top liner PBR at 2402m. Meanwhile tested cmt line to 345 bars 5 min." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Circulated 1 bottoms 2500 lpm, rotated string @ 20 rpm, torque 15-18 kNm." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 20 m³ of 1.65 SG Tuned Spacer E+ with mud pumps 2500 lpm @ 80-50 bar." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to cement unit. Released SSR dart. Started to mix the cement. Not able to add chemicals." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Troubleshot and found no communication between chemical injection software and mixing pump. Through phone call to Halliburton in town it was possible to reboot the software system and continue the operation." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Cemented 9 5/8' liner. Pumped 29.4m³ cement slurry 1.9 SG, 800 lpm @ 30-58 bar. Simultaneously rotated the liner during the cement job 20 rpm. torque 15-18 kNm. Displaced cement line to rig floor with fresh water. Closed Lo-torque valve on cement line. Bottom SSR plug sheared at 75 bar, after 28m³." "On 2007-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Displaced cement with 51.36 m³ (2341strokes) OBM at 2500 lpm, bumped plug, FCP 52 bar. Wiper plug sheared @ 1181 strokes and 250 bar. Rotated 20 rpm, final torque 20 kNm." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Applied 120 bar to plug, held for 5 min. Bled of pressure to the cmt unit, 700 l in returns." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3113m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Set TSP packer according to Weatherford procedure up/down weight 160/135 MT" "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressured up to 40 bar, pulled running tool out of the PBR. Pumped 80 m³ of 1.4 SG OBM 2500 lpm." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Broked connection and dropped 2 Halliburton sponge balls, continued circulate hole clean with 2500 lpm @ 95 bars. Approx. 2 m³ cement in returns." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flow checked well, static. Pumped 5m³ 1.60 SG slug." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2422m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to L/O cmt head." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1703m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH F/2422m T/1703m." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1703m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Commenced breaking down cmt head." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1703m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued L/O CMT head." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1703m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to POOH w/ 5½' and TSP packer running tool." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Continued POOH w/ 5½' and TSP packer running tool F/1703m T120m" "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Flow checked prior to pull BHA, well static." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH w/ TSP packer running tool and L/O same." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Cleared and cleaned rig floor. Made up bull nose jet sub, ran in and washed BOP, continued running in and washed Well head. Rotated string while washing 10-100 rpm, 2230-2500 lpm, 800-1200 Nm." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up and ran in with test plug and installed same in Well head." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Held tool box talk prior to commence BOP test." "On 2007-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 8.5 hours. Operational details: Flushed through choke and kill lines to BOP. Commenced BOP test 25/345 bars 5/10 min." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: POOH and laid out test assy. Checked seals on test plug, found in perfect condition. Cleared rig floor." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held tool box talk prior to leak test well. Lined up and leak tested 9 5/8' Liner and Liner Hanger 25/310 bars 5/10 min, w/ 1.4 SG OBM 4.3m³." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Bled of pressure through rig floor stand pipe manifold in stages. Total returns 3.75 m³." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: L/O 8 1/4' DC's and jar. Simultaneously tested stand pipe 25/345 bars 5/10 mins." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Continued testing of the stand pipe 25/345 bars 5/10 mins. Tested Choke manifold 25/345 bars 5/10 mins" "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to P/U 8½' drill assy." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Commenced P/U 8½' BHA. Simultaneously testing mainfold 25/345 bars 5/10 mins." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleared and cleaned rig floor." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Changed out saver sub and torqued to 87 kNm." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued P/U 8½' BHA and RIH F/0 T/ 43m. Loaded radio active source into Ecoscope." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 120m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Continued P/U 8½' BHA and RIH F/43m T/ 120m. Changed out master bushing to PS-21 slips." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 935m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: RIH w/ 8½' BHA on 5' DP F/120m T/935m." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 935m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: M/U to TDS and filled the pipe, tested the MWD tool @ 1700 lpm, 76 spm, 101 bars." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1342m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued RIH w/ 8½' BHA on 5' DP F/935m T/1342m, M/U to TDS and filled the pipe." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1342m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Performed choke drill. Held tool box talk w/ night shift prior to RIH w/ 8½' BHA on 5' DP." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1586m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued RIH w/ 8½' BHA on 5' DP F/1341m T/1586m, M/U to TDS and filled the pipe." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1586m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Changed out surface handling equipment to run w/ 5½' DP." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1586m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Trouble shot PS-21 slips, could not rectify problem in table, changed out slips to PS-30 slips." "On 2007-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1646m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Continued RIH w/ 8½' BHA on 5½' DP F/1586m T/1646m." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3038m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Continued RIH w/ 8½' BHA on 5' DP F/1646m T/3038m, filled pipe every 1000m." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: M/U to TDS and washed F/3038m T/ 3080m." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Changed out PS-30 to manual master bushing." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3086m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Started to wash down, tagged TOC @ 3086m. Up/down weight 167/135 MT 162 static." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3114m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Commenced to drill out 9 5/8' shoe track F/ 3086m. 50rpm, 2200 lpm, 12-16 kNm, weight RIH 147 MT." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3116m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drillied new formation from 3114 m to 3116 m with 60 rpm, 2000 lpm, max 20 kNm, SPP 180 bar." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3116m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Circulated to condition the mud to 1.4 SG prior to perform FIT. 60rpm, 2200 lpm, 12-15 kNm, 180 bar." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3105m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Lined up and pulled back into the shoe to 3105 m, closed annular. Performed FIT to 1.60 SG EMW, applied 56 bar to annulus and down DP w/ 1.40 SG OBM. Fluid pumped 780 ltr, fluid returned 740 ltr." "On 2007-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3157m. The activity was categorized as 'drilling -- drill' and lasted for 9.8 hours. Operational details: Drilled 8½' hole from 3116 m to 3157 m . Parameters: 2000-2200 lpm, 212 bar SPP 50-60 rpm, 13-19 KNm, 1-5 MT WOB, 2-6 m/hr ROP, 1.46 ECD." "On 2007-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 8½' hole from 3157 m to 3200 m . Parameters: 2000-2200 lpm, 210-211 bar SPP 60-130 rpm, 13-22 KNm, 1-5 MT WOB, 6-10 m/hr ROP, 1.46 ECD." "On 2007-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3457m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Continued drilling 8½' hole from 3200 m to 3457 m . Parameters: 2200 lpm, 208-215 bars SPP 130-140 rpm, 17-23 KNm, 3-8 MT WOB, 15-28 m/hr ROP, 1.46-1.47 ECD." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3480m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 8½' hole from 3457 m to 3480 m . Parameters: 2200 lpm, 208-215 bars SPP 130-140 rpm, 17-23 KNm, 3-8 MT WOB, 15-28 m/hr ROP, 1.46-1.47 ECD." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3441m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Wash pipe leaked. Pulled 1 stand up to 3441m and installed a pump in sub. Established circulation at 1900 lpm @ 205 bars. Had good returns over the shakers with cuttings." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3480m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Held tool box talk prior to change out wash pipe. Replaced wash pipe. M/U 1 stand of DP and established rotation at 60 rpm @ 1800 lpm and washed down to 3480m." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3520m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued drilling 8½' hole from 3480 m to 3520 m . Parameters: 2200 lpm, 214-217 bars SPP 140 rpm, 19-23 KNm, 3-6 MT WOB, 28 m/hr ROP, 1.47 ECD." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3520m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Commenced circulating well clean reciprocating and rotating the string with 2200 lpm @ 160-180 RPM up, 1800 lpm @ 80 rpm down." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3520m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Continued circulating the well clean while reciprocating and rotating the string, with 2200 lpm @ 160-180 RPM up, 1800 lpm @ 80 rpm down." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3158m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Flow checked well, well static. Simultaneously installed PS-21 auto slips & wiper rubber. POOH pumping 700 lpm from 3520m to 3158m." "On 2007-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3352m. The activity was categorized as 'drilling -- trip' and lasted for 10.0 hours. Operational details: Initiated Stethoscope and commenced taking pressure points according to Schlumberger procedure. Took 6 pressure points before midnight" "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3430m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Continued taking pressure points according to Schlumberger procedure. Took 3 pressure points before Geoservices unit did shut down." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3412m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Geoservices unit shut down due to activation of two gas detectors. The shut down was caused by water in one of the gas detectors. Re-booted the unit and the system." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Continued taking pressure points according to Schlumberger procedure. Took 6 pressure points." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3517m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Continued taking pressure point according to Schlumberger procedure. Took 1 pressure point." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3517m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Down linked MWD Stethoscope" "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3517m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flow checked well, well static." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3109m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Commenced pump out of hole from 3517m to 3109m, 700 lpm 31bars. Up/down weight 167/134 MT. Monitored well static." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3109m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Circulated bottoms up 2200 lpm 210 bars. Meanwhile serviced rig equipment." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3109m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Dropped 2 3/4' drift. Performed kick drill. Flow checked well, well static." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2916m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued POOH from 3109m (pulled 5 stds wet) to 3013m. Performed torque readings, 10 rpm 10.9 kNm, 15 rpm 11.7 kNM, 20 rpm 11.7 kNm, Weight of the string during rotation 147 MT. Took up/down weight 168/134 MT. Distance from neutral to up weight 0.6 m. Continued POOH wet from 3013m to 2916m." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1748m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Made up to TDS and pumped 5m³ 1.6 SG slug. Continued POOH from 2916m to 1748m. Draw work brake unable to release." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1748m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Investigated problem with draw work brake." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1586m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued POOH from 1748m to 1586m." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Changed out to 5' DP handling equipment. Continued POOH from 1586 to 130m. Rectified problem with draw work." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well, well static. Held tool box talk prior to L/O BHA." "On 2007-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Continued POOH w/ BHA and L/O same." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Cleaned and cleared rig floor. Function tested BOP." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Held tool box talk prior to R/U 7' liner handling equipment. R/U 7' liner handling equipment." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH w/ 7' liner." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: P/U shoe, float, and landing collar. Made up same with Bakerlock. RIH w/ 7' liner from 39m to 63m" "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued RIH w/ 7' liner from 63m to 147m, filling every 5th. joint." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 440m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Held tool box talk with day shift prior to RIH w/ 7' liner. Continued RIH w/ 7' liner from 147m to 440m, filling every 5th. joint. Problem M/U 7' liner joints." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 487m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Laid out 4 joints due to damaged threads and replaced w/ the 3 back-up." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 487m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Changed to 5½' DP elevators. P/U hanger/TSP packer assembly and made up same as per Weatherford procedure. Removed 7' FMS slips, installed master bushing. Filled PBR with Hi-visc mud. Took up/down weight 86/83 MT" "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 487m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: R/D Odfjell 7' casing tong. Removed HTS rollers, cleared and cleaned rig floor." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 487m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box prior to RIH w/ 7' liner on 5½' DP." "On 2007-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3036m. The activity was categorized as 'drilling -- casing' and lasted for 7.8 hours. Operational details: Installed PS-21 slips. Continued RIH w/ 7' liner on 5½' DP from 487m to 3036m, filling every 5th stand. Entered 9 5/8' liner @ 2404m without any obstructions." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3480m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Continued RIH w/ 7' liner on 5½' DP from 3036m to 3480m, filling every 5th stand." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3520m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Established circulation @ 500 lpm 34 bars. Continued RIH washing down w/ 7' liner on 5½' DP from 3480m and tagged TD at 3520m. Down/up weigth 144/187 MT." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Racked back one stand. Made up 3m + 2m pup joints." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up cement head and connected up to TDS. Ran and tagged bottom to verify TD at 3520m. Set down 3 MT. Picked to 1 meter to 3519m." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated 1½ open hole volume @ 1330 lpm 75 bars. Held pre-cement job meeting. Pressure tested cement line to Lo-torque valve at cement head." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Dropped ball and commenced setting the liner hanger according to Weatherford procedure." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Completed installation of the 7' line hanger." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Circulated 1 bottoms up @ 2000 lpm, 151 bars, 20 rpm, 17-18 kNm." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Pumped 15 m³ of 1.65 SG Tuned Spacer E+ at 1500 lpm with the mud pumps. Closed Top Drive IBOP. Maintained 20 bar above IBOP. Dropped bottom DPD #1 dart, good indication with flag. Pumped 12.7 m³ 1.90 SG cement slurry at 800 lpm, rotating the string 20 rpm 16-19 kNm. Displaced cement line to rig floor w/ 890 l fresh water. Dropped DPD #2 dart for releasing wiper plug. Displace cement with 41.5 m³ (1893 strokes) OBM at 1500 lpm, 20 rpm string rotation. Had max 25 kNm . Wiper plug bumped @ 1893 stroks, applied 170 bars to Wiper plug for verification. Bled off pressure and checked for backflow. No losses during the entire cement job." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed TSP packer according to Weatherford procedure. Up/down weight 175/140 MT" "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Circulated well clean w/ 1.4 SG OBM @ 1700-2200 lpm, 62-102 bars, total pumped 353m³. Had spacer and cement in returns." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3519m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Flow checked well. Well static. Meanwhile held tool box talk prior to L/O cement head." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2980m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Released running tool. L/O cement head pup joints and racked back one stand." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2980m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed 2 spong balls, made up string to TDS and pumped down the spong balls with 32m³ (string volume)" "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Pumped slug of 1.6 SG OBM. POOH w/ 7' TSP packer running tool from 2980m to 36m." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Removed PS-21 slips and installed master bushing. Continued POOH w/ TSP packer running tool and L/O same." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared & cleaned rig floor, checked dies in AFT PRS." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick BOP and WH clean out assy." "On 2007-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 330m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: M/U clean out assy. and RIH same to 330m. Positioned jet sub in WH at 138m and washed WH, Riser and BOP reciprocating the washing assy. across the specified areas. w/ 2500 lpm, 52 bars and 30 rpm." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 330m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Continued cleaning out the WH and BOP." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Laid out washing assy." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to change out handling equipment and picking up clean out assy." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed out handling equipment to 3 ½', dies in AFT AR, BX elevators inserts and insert of the PS-21.." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 280m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: M/U 7' liner clean out assy. w/ 6' bit and 7' scaper. RIH on 3½' DP from surface to 280m" "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 450m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued RIH with clean out assy. on 3½' DP from 280 to 450m" "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1062m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Changed elevator inserts to 5' DP. P/O 9 5/8' Razor Back Scraper pick up weight 80 MT. Re-dressed PS-21 and Iron roughneck to 5' DP. Removed HTS rollers. RIH with 5' DP from 465m to 1062m." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1062m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up 4½' IF to 5½' FH X-O. M/U string to TDS, filled string prior to pressure testing of the 7' liner." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1062m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Held tool box talk prior to pressure testing of the 7' liner. Spaced out to middle pipe rams. Confirmed line up, leak tested line up to 310 bars 5 mins. Pressure tested 7' liner pressuring up in increments to 310 bars, 10 mins." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1062m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Bled off pressure, had 4098 l in return. Broke out 4½' IF to 5½' FH X-O. Lined up to BOP." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1121m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: P/U Tie Back Mill. Held tool box talk prior to change out 5' handling equipment to 5½' handling equipment. P/U MFCT, Razor Back Scraper. Re-dressed PS-21 slips and elevators to 5½' DP. Checked flow rate/pressures. 58spm/103bars - 95spm/250bars." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2008m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Continued RIH with Clean out assy. on 5½' DP from 1121m to 2008m. Checked flow rate/pressures. 58spm/118bars - 95spm/247bars" "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Continued RIH with Clean out assy. on 5½' DP from 2008m to 3017m. Checked flow rate/pressures. 54spm(1240lpm)/104bars - 95spm(2101lpm)/254bars. Pumped 50m³ conditioned mud @ 106 spm, 2330 lpm 300 bars with 20 rpm 11 kNm. Took up/down weight 164/132 MT with pumps off." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3132m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued RIH with Clean out assy. on 5½' DP from 3017m to 3096m. M/U to TDS and scarped TCP gun hanger setting depth, from 3090m to 3125m with 100 spm, 300 bars, 40 rpm and 10-14 kNm. Rotation weight 147 MT." "On 2007-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3420m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued RIH with Clean out assy. on 5½' DP from 3132m to 3420m." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3457m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: M/U to TDS, confirmed depth with tally. Pumped 1196 lpm / 120 bars, 2016 lpm / 260 bars and 2120 lpm / 289 bars, at 40 rpm. Scraped from 3427m to 3457m bit depth = 2970m to 3000m scraper depth. Up/Down weight 174/139 MT." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued RIH from 3457m and tagged top of 9 5/8' PBR at 2405,5 m (3473.8m bit depth). Picked back rotated string at 50 rpm - 50 spm - 92 bars and 11-14 kNm. Slacked off slowly w/ 50 RPM with the Top Dress Mill assembly and set down 1-2 tonn on top of the PBR for a few minutes. Pulled out of the PBR with rotation." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3468m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pulled bottom of polish mill 5 meter above liner top and reciprocated the string while conditioning the mud 40 rpm, 96 spm(2100lpm), 291 bars," "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3468m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Sheared MFCT by setting down 24 MT on PBR with top dress mill. Opened the circulation ports. Established circulation of 191 spm(4200lpm) 230 bars, 40 rpm, 9 kNm kept 6.8 MT down weight." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3468m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to clean out services lines." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3468m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Commenced cleaning of surface equipment with Base oil then soap pil." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 6.2 hours. Operational details: Continued cleaning of surface equipment. Meanwhile injected slops." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Filled sandtraps with base oil from pit # 10 & circulated through lines in shakers with base oil." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Mixed soap pill in pit # 10, flushed soap pill through all possible surface lines at maximum rate of 4000 lpm." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Held tool box talk prior to prepare fluid used for well clean out. Prepared treated SW, pills and cleaned pits. Meanwhile closed bag and opened piperam. Pulled up +/- 1m to close MFCT." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Prepared seawater pre-mix prior to displacement." "On 2007-08-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Started displacing well with soap train to MFCT at 1000 lpm up chokeline. When pill at bit DP pressure reading:230 bars." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued displacing well with soap train to above MFCT at 1000 lpm, 230 bars constant DP pressure up choke line." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Stopped pumping. Closed in the well with 200 bars DP, 170 bars choke pressure. Opened MFCT setting down weight." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Circulated well at 2800 lpm, holding choke pressure constant at 170 bars. New DP pressure 270 bars. Continued circulating 2800 lpm 270 bars constant DP pressure w/ treated sea water" "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed in well @ 80 bars when treated sea water at surface. Bled off the pressure from 80 bars in two steps to zero, prior to taking inflow test over the trip tank. Lined up to trip tank." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Inflow tested well over the trip tank for 30 mins. - OK" "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3470m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Spaced out and closed pipe rams. Pressure tested well 20/345 bars 5/10 mins with treated sea water. Simultaneously mixing for displacing the well with treated sea water below 100 NTU" "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued to clean surface lines. Prepared to pump TSW." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3474m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: With MFCT in open position, pumped TSW at 3400 lpm / SPP 284 bar. Total volume pumped 365 m3. NTU reading levelled out at approx 150." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3177m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Closed MFCT. POOH with cleaning assembly on 5 1/2' DP from 3474 m to 3177 m MD. Observed 12 mm locking nut falling from derrick, halted operation." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3177m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Performed FG inspection in derrick. Lock nut traced to clamp on ladder to crown block." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1080m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Continued to POOH with cleaning assembly on 5 1/2' DP from 3177 m to 1080 m MD." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1080m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed from 5 1/2' to 5' handling equipment." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1062m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out and laid down 14' Razor back assy #5 and Tie-back/top dress mill assy #4." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 465m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued to POOH on 5' DP from 1062 m to 465 m MD. Changed inserts and jaws on IR to 3 1/2' DP. Changed to 3 1/2' inserts in elevator." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 465m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke out and laid down 9 5/8' Razor back assy #3." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 14m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: POOH with cleaning assy on 3 1/2' DP from 465 m to 14 m MD." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke out and laid down 7' Razor back assy #2. Laid out assy #1, pup with 6' bit. Changed to 5 1/2' handling equipment." "On 2007-08-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up Wear Bushing Running and Retrieving Tool (WBRRT) to stand of 5 1/2' HWDP. Checked tool." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with WBRRT on 5 1/2' HWDP. Checked serial numbers of HWDP on way in. Found deviation in tally on joint #7 / std#2, serial number was incorrect compared to tally. Control measured joint and found a lenght deviation of 4,5 cm compared to tally." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with WBRRT on 5 1/2' HWDP while measuring lenghts on all joints. Found several lenght deviations ranging from a few mm to mamximum 11 cm. Found one more wrong serial number." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Latched onto WB at 139,5 m MD and pulled same with 25 MT overpull. Broke circulation and washed across wellhead with 3000 lpm using TSW." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with WB/WBRRT on 5 1/2' HWDP. Control measured 6 more 5 1/2' HWDP joints on way out. Recalculated total tally with new measures and found a deviation of only 2 mm." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Rigged up casing tong, flush mounted spider and elevator for running 9 5/8' x 10 3/4' tie-back casing." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox meeting prior to start running 9 5/8' x 10 3/4' tie-back casing." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- casing' and lasted for 10.8 hours. Operational details: Ran 9 5/8' tie back casing to 798 m MD." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held toolbox talk prior changing elevator. Changed elevator from 9 5/8' to 10 3/4' BX3. Found leakage on hydraulic fitting on 10 3/4' BX3 elevator." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed hydraulic fitting and bolt head connection for return line on 10 3/4' BX3 elevator." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 811m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up and made up 9 5/8' x 10 3/4' x-over. Changed slips segments in flush mounted spider. Hung off on x-over and installed casing swage on top of 10 3/4' casing." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Slip and cut drilline." "On 2007-08-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Performed 6 monthly maintenance and inspection of crown block." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 811m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Removed block hang off sling. Calibrated block." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 811m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held toolbox talk prior to recommencing casing running. Broke off and laid down casing swage." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1141m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Continued to run 10 3/4' casing from 811 m to 1141 m MD." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2262m. The activity was categorized as 'drilling -- casing' and lasted for 12.5 hours. Operational details: Ran 10 3/4' tie-back casing from 1141 m to 2262 m MD. Average running speed 8 jnts/hr." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2262m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed from 10 3/4' BX3 elevator to 5 1/2' DP elevator." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2262m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up and made up 10 3/4' casing hanger complete with isolation sleeve and PADPRT tool" "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2262m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed spider from rotary and installed bushings. Removed casing tong." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 10 3/4' casing/hanger on 5 1/2' HWDP landing string. Strapped pipe on way in." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2408m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up TDS. Took up/down weights 253/199 MT. Pumped at 450 lpm while running in slowly with landing string. Observed pressure bulid up and lost returns at 2406,4 m MD indicating seals engaging 9 5/8' liner sealbore. Stopped pumps. Observed stinger shroud shearing some 1,20 m further in and got hanger landing depth 0,8 m (total of 1.2+0.8=2m) further in at 2408,4 m MD." "On 2007-09-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2408m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed low pressure test of stinger seals to 70 bar / 10 min - ok." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2408m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Marked pipe with 72 MT and 128 MT hookload. Applied 7 MT on PADPRT tool and rotated 4 1/4 turn clockwise to set tool. Pipe dropped 8,5' as intended. Closed UPR." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2408m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held toolbox talk prior to setting MS seal. Pressured up to 207 bar with cement unit through kill line for 10 mins to set the MS seal. Volume pumped 272 liters." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Opened UPR and pulled 50 MT above landing string weight to unset PADPRT tool. Pressure tested MS seal to 35/345 bar 5/10 mins. Volumed pumped 447 liters." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with PADRT tool on 5 1/2' HWDP. Laid down PADPRT tool." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Closed shear ram and lined up to pressure up underneath with cement unit. Pressured up with cement unit to 345 bar. Pumped a total of 2630 liter on 1st attempt, good correlation with theoretical volume. Observed trendline which did not stabilize - steady drop observed at around 1 bar/min. Pressured up twice to 345 bar - same trend observed. Total volume pumped 2860 liters Attempted to bleed pressure back to cement unit - nogo, kill line blocked for unknown reason. Bled back to trip tank and recovered 2500 liters. Decided to re-attempt pressure test up cement line." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up from cement unit pumping up cement line. Flushed through and performed line test to 345 bar - ok." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Troubleshot leakage in well. Pressured up on well to 345 bar from cement unit through cement line. Similar trendline observed with leakage rate of 0,5-1 bar/min. Pressured up on well twice more. Bled off pressure rapidly and lined back to cement unit. Pressure on cement unit rose from 2,8 bar to 7 bar over 2 hrs. Meanwhile discussed situation and way forward. Prepared for running MS seal retrieval tool." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Picked up MS seal retirevel tool and inspected seals. RIH with retrieval tool on 5 1/2' HWDP landing string as per Vetco procedure. Engaged tool by 1/2' turn lefthand. Set down landing string weight of 10 MT instead of the intended 3 MT. Adjusted string weight and string jumped approx 0,3 m, got sudden gain in trip tank of approx 250 liter. Closed annular and pulled MS seal free with 10 MT overpull. POOH with retireval tool and MS seal on 5 1/2' HWDP. Backed off MS seal, re-set running tool and laid down same." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Inspected MS seal and found scores on seal. Discussed situation. Prepared hanger jet and wash tool." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Picked up and made ut Vetco jet and wash tool. RIH with tool on 5 1/2' HWDP landing string. Tagged top of 10 3/4 casing hanger. Washed seal area, rotated with 3 rpm while pumping at 2200 lpm. POOH with jet and wash tool. Discussed way forward." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Prepared for running WBBRT w/10 3/4' wearbushing. Picked up WBRRT, checked tool and installed 10 3/4' wearbushing. RIH with tool WBRRT/wearbushing on 5 1/2' HWDP landing string." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Set wearbushing at 140,2 m MD. POOH with WBRRT and laid down tool." "On 2007-09-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Hung off RTTS in rotary and made up to stand of 5 1/2' HWDP. Installed automatic slips." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1650m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 9 5/8' RTTS on 5 1/2' DP/HWDP to 1650 m MD." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1650m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Took up/down weights 132/117 MT. Roateted string to set RTTS packer. Slacked of 30 MT on the running string and set packer at 1650 m MD. Lined up to pump from cement unit up cement line and standpipe. Closed standpipe valve and performed line test to 345 bar - ok." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1650m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pressurised well below RTTS packer in 50 bar increments. Held each step for 10 mins. Good tests obtained at 50, 100, 150, 200, 250 bar - no gain in trip tank observed. Total volume pumped at 250 bar was 1129 liter." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1650m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: At 300 bar leakage was observed, pressure dropped 7 bar / 10 min - also gained 40 liters in triptank over 10 mins. Volume pumped 1332 liter. Bled off pressure on well." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Released RTTS. POOH on 5 1/2' DP/HWDP with RTTS. Removed automatic slips and master bushing. Laid down RTTS." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Picked up WBRRT set in retrieval mode. RIH with WBRRT on 5 1/2' HWDP landing string. Latched on to 10 3/4' wearbushing at 140 m MD and pulled free with 40 MT overpull." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2408m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up PADRT tool set in catch mode. RIH on 5 1/2' HWDP landing string and latched on to 10 3/4' hanger according to Vetco instructions." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2268m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up with 255 MT hookload and POOH with 9 5/8' x 10 3/4' tie back casing on 5 1/2' HWDP landing string. Removed master bushing." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2268m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Held toolbox talk prior to rigging 10 3/4' casing handling equipment. Installed casing tong, BX3 elevator and spider." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2265m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to laying down 10 3/4' casing hanger / casing. Broke and laid down hanger and PADRT tool." "On 2007-09-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1670m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: POOH with 10 3/4' tie-back casing from 2265 m to 1670 m MD. Average pulling speed 11 jnts/hr." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 822m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: POOH with 10 3/4' casing from 1670 m to 822 m MD. Average pulling speed 13 jnts/hr." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued pulling 10 3/4' casing from 822 m to 798 m MD. Hung off on x-over. Broke out and laid down 9 5/8' x 10 3/4' x-over. Changed to 9 5/8' elevator." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 550m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: POOH with 9 5/8' casing from 798 m to 550 m MD." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 550m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed dies in casing tong from 9 3/4' to 9 5/8' (arrived on boat)." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Continued to POOH with 9 5/8' casing from 550 m to 40 m MD." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed spider and installed master bushing. POOH from 40 m MD. Laid down seal stinger. Inspected seals, lower seals missing and significant damage to rest of seals." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tolbox talk prior to breaking back up TSP assembly. Cleared and tidied drillfloor. Changed to 5 1/2' inserts in elevator." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Picked up TSP assembly. Broke 9 5/8' connection and installed by pass ball drop seat. Re-made 9 5/8' connection and laid down tool on pipedeck." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Picked up WBRRT. Broke out jet sub and configured tool for BOP testing. RIH with WBRRT and 14' wearbushing on 5 1/2' HWDP landing and set same in wellhead." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke TDS connection and parked travelling block for maintenance." "On 2007-09-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: Pressure tested BOP to 35/345 bar 5/10 min according to Mærsk USP." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.5 hours. Operational details: Pressure tested BOP to 35/345 bar 5/10 min according to Mærsk USP." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Released WBRRT and POOH with same on 5 1/2' HWDP landing string. Re-set tool on surface. Laid down WBRRT on pipe deck. Meanwhile function tested shear ram." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up 9 5/8' x 14' TSP assembly with simultaneous lift on elevator and deck crane. Inspected seals. Hung off assy in rotary. Removed masterbushing and installed automatic slips. RIH with TSP on 5 1/2' DP to 100 m MD." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2397m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: RIH with TSP assy on 5 1/2' DP from 100 m to 2397 m MD. Running speed limited to 2 mins/std." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2412m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Dropped 1 3/4' aluminium ball. Took up/down weights 160/131 MT. Continued to RIH with TSP packer from 2397 m ti 2412 m MD. Applied 10 MT on TSP assy. Pressured up string to 230 bar / 440 lpm. Observed pressure for 5 mins. Increased pressure and observed shear at 268 bar." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2408m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pulled out 4 m and set packer by applying 40 MT on top of PBR. Adjusted weight to 10 MT. Verifed new top of PBR to 2398.05 m MD." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2408m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed UPR, lined up from cement unit to BOP, and pressure tested TSP packer and annulus to 180 bar - ok. Volumed pumped 1632 liters." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2350m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: POOH with TSP setting tool on 5 1/2' DP from 2408 to 2350 m MD. Observed hydraulic leak on aft PRS." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2350m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Repaired hydraulic leak on aft PRS." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Continued to POOH with TSP setting tool on 5 1/2' DP from 2350 m to 200 m MD." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk. Removed automatic slips from rotary." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued to POOH with TSP setting tool from 200 m MD to surface. Laid down tool in basket on main deck." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with WBRRT on 5 1/2' HWDP landing string. Latched on to 14' WB at 140 m MD and pulled free with 30 MT overpull. Washed across subsea wellhead with 3000 lpm. POOH with WB/WBRRT on 5 1/2' HWDP landing string." "On 2007-09-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Laid down WBRRT. Installed swedge and tested IBOP valves on TDS and standpipe valve to 35/345 bar 5/10 mins. Meanwhile : -Backloaded used casing. Loaded, tallied and laid out new casing in stb pipedeck bays. -Repaired hydraulic hose on topdrive -Tested valves on kill manifold to 35/345 bar 5/10 mins." "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Rigged up casing OWS casing tong. Changed inserts in elevator. Redressed PS-21 slips. Meanwhile : -Backloaded used casing. Loaded, tallied and laid out new casing in stb pipedeck bays." "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Backloaded used casing. Loaded, tallied and laid out new casing in stb pipedeck bays. Meanwhile : -Barriered off drillfloor and commenced service on forward PRS" "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 0.5 hours. Operational details: Had to halt loading casing temporarily. Supply boat Island Frontier reported trouble which could affect station keeping. Boat pulled away temporarily." "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: Loaded, tallied and laid out new 10 3/4' casing in aft stb/port bays. Produced running tally. Counted joints on deck. Meanwhile : -Pressure tested choke manifold to 35/345 bar 5/10 mins -Pressure tested TIW and gray valve to 35/345 bar 5/10 mins" "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke down TIW and Gray valve after pressure testing same." "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 7m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to running 9 5/8' x 10 3/4' tie-back casing. Picked up seal stem assy. Commenced to run in hole with 9 5/8' casing. Got problem closing/functioning elevator. Halted operations to remedy situation." "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 7m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Changed hydraulic fitting on BX elevator." "On 2007-09-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 374m. The activity was categorized as 'drilling -- casing' and lasted for 8.2 hours. Operational details: RIH with 9 5/8' tie-back casing from surface to 374 m MD. Observed high thread torque on several joints.Observed some dry boxes. Had to lay out joint #57, #52 and #48 due to 70% thread torque on JAM unit and damaged threads. Used contingency dope LubeSeal API mod as required on pin end after joint #48. Average running speed less 4 jnts/hr." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 9 5/8' tie-back casing from 374 m to 798 m MD. Washed pin ends and applied contingency dope as required. Average running speed 6 jnts/hr." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 796m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed to 10 3/4' BX3 elevator. Picked up and made up 9 5/8' x 10 3/4' x-over." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 796m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held toolbox talk. Removed PS-21 slips and changed to 10 3/4' inserts, put slips back in rotary. Repositioned rollers on HTS. Adjusted PDM head." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1505m. The activity was categorized as 'drilling -- casing' and lasted for 7.2 hours. Operational details: Held toolbox meeting prior to running 10 3/4' tie-back casing. Ran 10 3/4' casing from 796 m to 1505 m MD. Average running speed 8 jnts/hr. Experienced problems with HTS conveyer belt." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1505m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Repaired conveyer belt." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1920m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Continued to run 10 3/4' tie-back casing. Average running speed 10 jnts/hr. Monkey arm on HTS jammed in upper position." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1920m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Mærsk ET techican fixed problem on software." "On 2007-09-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2253m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Continued to run 10 3/4' tie-back casing from 1920 m to 2253 m MD." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2258m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Picked up 6,05 m 10 3/4' pup joint made up and RIH with same. Changed elveator. Picked up 10 3/4' casing hanger, washed, inspected and doped threads. Made up 10 3/4' casing hanger. Checked tally and counted joints left on deck - ok." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2258m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged down casing tong. Removed casing slips. Checked PADPRT tool." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2385m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 9 5/8' x 10 3/4' tie-back casing, hanger and PADPRT tool on 5 1/2' HWDP landing string. Set depth counter at 2385 m MD. Took up and down weights 250/200 MT." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2402m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Brought pumps up to 350 lpm and ran in hole with tie-back casing. Observed pressure increase and loosing weight at 2399 m MD. Stung approx 1 m further in and PBR locator in sealstem sheard out. Total sting in 2,7 m. Landed hanger at 140,1 m MD as per Vetco datum." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2402m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to pump from cement unit up kill line through TDS. Performed low pressure test on sealstinger to 70 bar/10 min - ok. Recorded on chart." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2402m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Adjusted block weight to 73 MT. Rotated string 4 turns clockwise to activate PADPRT tool, observed 8,5' drop as intended. Closed UPR and pressured up above PADRT tool to 207 bar to set MS seal - ok." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: With UPR closed, pressure tested MS seal from above to 35/345 bar 5 /10 min - ok. Released PADPRT tool according to Vetco instructions and POOH with same on 5 1/2' HWDP landing string." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Flushed lines. Closed Shear ram. Pressure tested 9 5/8' x 10 3/4' tie-back casing and sealstem/PBR to 35/345 bar 5/10 min - ok. Pumped and bled back a total of 2637 liter, good correspondance with theoretical volume." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picked up 10 3/4' lock down sub and RIH on 5 1/2' HWDP landing string to 140 m. Set same according to Vetco instruction. Closed UPR and pressure tested lock down sub to 345 bar/10 min." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with RT on 5 1/2' HWDP landing string." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Tidied drillfloor and removed casing running equipment for backload." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held toolbox talk. Picked up special 9,567' casing drift and RIH with same on 5 1/2' DP to 200 m MD." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1590m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Installed automatic slip. RIH with drift on 5 1/2' DP and drifted well down to 1590 m MD. Observed 1-3 MT drag from 1439 m to 1536 m MD." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: POOH with casing drift on 5 1/2' DP and laid down same." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Built stand of 5 1/2' HWDP." "On 2007-09-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 642m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Picked up 10 3/4' GTV plug assembly. RIH with GTV plug on 5 1/2' HWDP/DP to 641 m MD. Measured 2 stands while running in. Took up/down weights 102/98 MT. Set GTV plug by applying clockwise rotation and alernating up down loads. Plug setting depth 641 m MD (mid packer element)." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 642m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Lined up from cement unit and performed line test to 345 bar/10 min - ok. Pressured up below GTV plug through DP and tested to 345 bar/10 min. Pumped 2150 liter with good correpsondance to theroretical volume. Recovered only 1800 liter. Discussed situation. Decided to move ahead with operations." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Released from GTV plug and pumped 10 m3 hi-vis on top of plug. POOH with GTV plug setting tool on 5 1/2' HWDP/DP. Laid down setting tool." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed shear ram and lined up cement unit to pump in BOP. Pressure tested above GTV plug to 345 bar / 10 min - ok. Volume pumped / bled back 863/830 liters." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up stand of drillpipe. Emptied BOP for water by blowing air down the DP." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed elevator and prepared slings for pulling diverter." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Continued preparing for releasing and pulling diverter." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pulling diverter." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Attempted to pull diverter - nogo - stuck in diverter housing. Removed lid to access lock dogs. Inspected locks and found chunks of metal in cavities, verified lock dogs free to move. Adjusted elevation. Worked diverter up and down. Diverter came free. Lifted out and set down on drillfloor." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared drillfloor. Transferred Claxton tool to drillfloor." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox meeting prior to nippling BOP overshot. Meanwhile worked on FWD PRS." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: Attempted to release lock ring on overshot. Used, C-spanner, chain hoists slings" "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Sourced torque tool for relasing flange on top of annular BOP instead of lock ring. Attempted to break bolts on flange - negative. Reverted to plan for releasing lock ring. Meanwhile reinforced C-spanners in mechanical workshop and continued work on PRS." "On 2007-09-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Worked to release overshot lock ring. Used C-spanner, chain hoists and slings. Meanwhile worked on FWD PRS." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Worked to release overshot lock ring. Used C-spanner, chain hoist. Rigged up eagle clamp and sheave. Pulled on lock ring C-spanner with tugger. Lock ring came free and was unscrewed by hand. Total thight turns approx 2,5. Meanwhile worked on FWD PRS." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed tools and slings from BOP. Attached sling to overshot and lifted same to drillfloor with tugger. Installed masterbushing, bushings and hole cover." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared for skidding BOP. Released NT-2 connector and removed obstacles in moonpool. Cleared and tidied drillfloor." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Continued nippling down BOP. Prepared for skidding BOP. Got problems with hydraulics on BOP trolley." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot problems with BOP trolley." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Skidded BOP on trolley and landed same on test stump." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Helt toolbox talk prior to running Claxton tool." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Picked up Claxton tool and made up to stand of 5 1/2' HWDP." "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Held toolbox talk. Landed Claxton tool i NT-2 connector on HPDR. Made up Claxton tool to NT-2 with Hytorq tool. Applied 2700 ft lbs on studs. Weather at 1430 : Wind 19 m /s Hs 3,8 / max 7,5" "On 2007-09-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: Watied on weather. Meanwhile worked on PRS." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Watied on weather. Meanwhile prepared for tranferring tension to block. Removed scaffolding and secured hatches on Centralizer deck. Weather at 0100 : Wind 9,7 m /s Hs 2,8 / max 4,1" "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held prejob meeting on Centralizer deck. Bled off pressure on tension cylinders and transferred 60 MT tension to block. Disconnected tension cylinder 1 and 3. Landed tensioner assembly on wooden chucks." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Disconnected cylinder 2 and 4 from tensioner assembly. Dismantled tensioner assembly. Removed tension ring. Removed boat collision stool and centralizer. Installed protector guides on Centralizer deck and landed tension ring in same. Installed protector guide on Tensioning deck. Meanwhile deployed hotstab on tuggerline through slot F-1. Engaged hotstab in hydraulic receptacle on TBC. Weather at 0600 : Wind 6,7 m /s Hs 2,2 / max 3,4" "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed scaffolding on Weatherdeck due to potential clash with HPDR riser. Tidied Centralizer deck." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on weather." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to disconnecting HPDR from wellhead." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Set valves on HPDR TBC. Set down weight to 55 MT. Pressurised primary unlock on TBC through minireel and hotstab. Lifted clear of wellhead/template in one continuos stroke. Hung of on handling sub, broke off and set back 5 1/2' DP stand. No VX-ring observed on wellhead - assumed still contained in TBC." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior installing riser spider." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed bushings. Installed riser spider." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: POOH with Tension joint and BOP joint double. Hung off in riser spider. Broke connection according to Vetco/Bandak procedure. Attached soft sling. Observed damage on soft slings. Halted operation to assess situation." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 121m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Inspected and rejected both soft sling. Searched for alternative slings - none onboard with sufficient SWL/lenght." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Slung Tension joint with 50 mm steel sling. Lifted same from drillfloor using deck crane. Laid down Tension joint in make up cradle on pipedeck." "On 2007-09-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 56m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: POOH with 22' HPDR. Removed fairrings while pulling out. Broke connections according to Vetco/Bandak procedure. Laid down doubles in port side storage rack." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Broke last connection between last doble and TBC joint. Laid out last double and put in port side storage rack. Pulled TBC joint. Inspected lock cavity on TBC, no VX-ring recovered. Slung TBC joint with heavy lift sling and laid down same on pipedeck. Secured rotary. Tidied drillfloor." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Brought 4 tension cylinder to drillfloor. Prepared for mounting cherry picker." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 1.0 hours. Operational details: Not allowed access in wellhead module due to ongoing pressure testing on gas lift system. Discussed situation and adjusted barriers accordingly. Meanwhile mounted cherry picker on drillfloor." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Transferred 4 tension cylinders from drillfloor to Tensioning deck. Meanwhile mounted cherry picker on drillfloor." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Dismounted/mounted cylinders on Centralizer deck with tugger support from moonpool. Meanwhile mounted cherry picker on drillfloor." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 7.0 hours. Operational details: Continued to dismount/mount tension cylinders in Tensioning deck roof. Used tugger support from moonpool for lifting cylinders." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Prepared for running production riser. Made up Tension joint handling tool to 6 m pup joint. Configured riser spider for running production riser. Prepared tension ring and protector guide in wellhead module." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed SJA / toolbox talk prior to running production riser." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Picked up TBC joint and hung off in spider. Removed handling tool. Picked up lower pup joint and landed same on TBC joint. Made up flanged connection according to Vetco/bandak procedure. Installed fairring accross connection." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Placed TBC in in level with scaffolding on Weatherdeck. Function tested TBC according to Vetco instruction. Installed dummy stabs. Oriented lock/unlock panel to 45 deg starboard aft." "On 2007-09-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Removed handling tool on production riser flange in riser spider. Lifted 1st double with dual lift on block and deckcrane. Made up flanged connection according to Vetco/Bandak procedure. Installed fairring on coupling. Ran in and placed TBC connector in level with Centralizer deck. Prepared guidewires in slot F-11 and F-13. Built scaffolding/barriers around deck openings." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Attached ROV hooks to guide slings. Made rope loop for retrieval of ROV hooks and guide sling clamp. Hauled guidewires with ROV hooks through Centralizer deck, ran to sealevel. Landed 1 st double in riser spider. Ran guidewires individually to 20 m above seabed." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed handling tool. Lifted 2nd double to drillfloor with dual lift on block and deck crane. Made up flanged connection according to Vetco/Bandak procedure. RIH with 2nd double. Meanwhile hooked up hydraulics on tension cylinders." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Lifted 3rd double to drillfloor with dual lift on block an deck crane. Removed handling joint. Made up flanged connection according to Vetco procedure. Meanwhile hooked up hydraulics on tension cylinders." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lifted tension joint to Horizontal position. Hoisted handling flange with 6 m pup joint to horizontal posistion with tuggers and made up to tension joint. RIH with 3rd double and landed in spider. Prepared for lifting tension joint to vertical position." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Lifted tension joint to vertical position and MU tension joint flange to upper pup joint." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Split riser spider and removed same." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH with tension joint and installed master bushing. MU 5 1/2' landing stand to handling sub." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared ROV to assist landing of PR. Verified that the VX-ring had been installed and checked F-12 well head." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed guidewires and lined up to 18 3/4' sub sea WH. Hook load prior to landing was 97 MT." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Installed hot stab in receptacle A and set valves on TBC locking panel to 'primary lock' position using ROV. Landed TBC on 18 3/4' WH and sat down 15 MT." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Prepared to set TBC according to Vetco procedures. Pressurized the TBC to 2500 psi using pump and minireel in moonpool. Did not get alignment indicating proper locking of TBC." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Had shut down for Siemens 'shut down and fire pump logic' (ESD tests)." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Unlocked TBC and repeated connetion procedures according to Vetco instructions. Pressurized the TBC to 3000 psi using pump and minireel in moonpool. Got alignment indicating proper locking of TBC. Sat all valves on lock panel A into 'parking position'. Performed 20 MT overpull test on H4-MUSL connector (TBC) with TDS. Slacked off to 10 MT overpull. Sat TBC valves on flush panel B to 'lower dog flush'." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Had shut down for Siemens 'shut down and fire pump logic' (ESD tests)." "On 2007-09-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed centralizer and boat collision stool on centralizer deck. Prepared for skidding cantilever." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Continued to install centralizer and boat collision stool on centralizer deck. Meanwhile had shut down for Siemens 'shut down and fire pump logic' (ESD tests). Restarted all systems." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed bleed off valve on tension joint and lined up to fill riser. Held tool box meeting prior to filling riser and performing pressure test. Filled riser using CMT pump and venting air through valve on tension joint. Kept 10 MT overpull on PR." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Performed pressure test of PR to 20 bar/5 min. Volume pumped 70 ltr. Attempted to move TDS to keep tension in PR during pressure testing." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Software problem on TDS (drawworks)." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressured up PR riser against well/GTV plug to 200 bar and compensated TDS to keep riser in tension. Performed pressure test of PR to 200 bar/10 min. Volume pumped 440 ltr." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared to pumpe corrosion inhibitor through port B1 on TBC using minireel and Vetco pump. Meanwhile finished installing centralizer and boat collision stool on centralizer deck" "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: MU tensioner ring assembly on centralizer deck. Meanwhile prepared rig for skidding and changed liners and piston fluid ends in MP2." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Commisioned all 4 new tension cylinders." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 9.5 hours. Operational details: MU tensioner ring assembly on centralizer deck. Meanwhile retrieved riser guide wires from wellhead template and performed area inspection for high wind forcast procedure." "On 2007-09-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Removed security bolt on RT from PR and POOH. LD RT and 20 ft pup joint. Installed hatch on F-12 and suspended operation to F-7." "On 2007-10-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.8 hours. Operational details: Prepared Rig for skidding and skidded rig from F7 to F12." "On 2007-10-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Skidded the cantilever 1.5 metres to SB." "On 2007-10-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered down the well head valves." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.2 hours. Operational details: Prepared main deck for skidding." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Held tool box talk prior to skidding of the cantilever." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.8 hours. Operational details: Skidded cantilever from F-15 to F-12" "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.8 hours. Operational details: Installed stairs to the cantilever. Removed well head hatches." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared for pick up the surface riser." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up the surface riser." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up the surface riser, removed protector. Meanwhile built scaffolding in the moon pool." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Removed the master bushing, ran in with the surface riser. Meanwhile built scaffolding at the well head deck." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Cleaned the NT2 well head connector. Landed and made up the surface riser." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to nippling up the BOP." "On 2007-12-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Prepared for nippling up the BOP, moved the BOP from the set back stump." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Moved the tension cylinders aside to be able to move the BOP in position over the surface riser. Aligned the BOP and the surface riser and landed the BOP. Meanwhile picked up and prepared the diverter for installation." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Installed the tension cylinders. Pressure tested the stand pipe manifold 20/345 bar 5/10 mins." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.8 hours. Operational details: Nippled up slick jnt, diverter and torqued up the BOP/Surface riser NT2 connector. Rigged down the diverter handling equipment. Pressure tested IBOP to 20/345 bars 5/10 mins." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Held tool box talk prior to pressure test the BOP, surface riser and the well head connection against GT plug. Pressure tested same to 20/200 bars 5/10 mins." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to installation of the Bowl Protector." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Rigged 5½' DP handling equipment and made up slick joint." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up Bowl Protector running tool." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH and installed the Bowl Protector at 20.9 m. Success on second attempt." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to retrieve the Annulus Insert in Subsea WH. Uncertainty with regards to length of landing string" "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Made up the Annulus Insert retrieving tool. RIH with the Annulus Insert retrieving tool on HWDP. Slow operation to get correct landing string lenght." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: RIH and tagged the Annulus Insert at 139.9 m. Pulled back 1.24 m took over pull of 40 MT. Attempted pass obstruction by turning the string 90º and 180º. Rotated the string with 2 RPM, passed obstruction." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with the Annulus insert retrieving tool for inspection." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Inspected the Annulus Insert retrieving tool. Found lock pin slightly bend but still operational." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 122m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH with the Annulus Insert retrieving tool from surface to 122 m." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Took parameters prior to engage and retrieve the Annulus Insert. Open annular up/down weight 82/79 MT / 4 RPM / 400 Nm. Closed annular up/down weight 82/79 MT / 4 RPM / 400 Nm." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH from 122 m and tagged the Annulus Insert at 139.9 m, set down 2 MT." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Rotated string and entered the J-slot. Set down 2 MT." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Closed annular and confirmed the engagement of the J-slot with 1 MT over pull. Marked string and turned string 3 turns to the left. Keeping the weight below 1½ MT set down weight and torque below 2 kNm. Marked string and measured 3 turns = 1¼'." "On 2007-12-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Monitored for possible annulus pressure." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Rotated the string 3 + ½ turn to the left, kept the weight below 1½ MT set down weight and torque below 2 kNm. Marked string and measured 3(½) turns = 1¼'. Total backed out with the Annulus Insert = 2½'. Corrected according to Vetco procedure." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Pulled back from 139.9 m to 138 m. Took weight at 138.6 m 10 MT. Rotated the string and passed the obstruction." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Displaced the riser to completion fluid at 1000 lpm / 1.5 bars. Total volume pumped 30 m³." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH with the Annulus Insert. Inspected the Annulus Insert. Found no damage." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up HWDP stand and measured from mark when engaged the Annulus Insert. Accumulated length 140.01 m." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to run and retrieve the Bowl Protector in surface WH." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up and made of the Bowl Protector retrieving tool." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH with Bowl Protector retrieving tool and set down at 20 m. Attempted to work string down to 20.9 m as Bowl Protector was reported installed previous to day. POOH after 2 attempts." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: OOH with Bowl Protector retrieving tool. Inspected the tool found no marks. Measured length from landing shoulder to Bowl Protector retrieving tool nose = 0.8 m. Painted landing shoulder white. RIH with Bowl Protector retrieving tool. Tagged at 20 m. Turned one round to the right. POOH with Bowl Protector retrieving tool and retrieved the Bowl Protector." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH with Jetting sub and commenced washing the surface well head area." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Washed the surface well head area. 2200 lpm used 20m³ completion fluid. POOH with Jet washing assy. and laid out same." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and cleared the rig floor." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk prior to make up Spear assy. Made up Spear assy and racked back in derrick." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Rigged up 10 3/4' casing handling equipment." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Tool box talk prior to make up and run 10 3/4' Tie- back assy." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: No crane available due to Helicopter. Meanwhile positioned the MST seal running tool on the rig floor. Inspected the MST running tool and confirmed leakages." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Made up Drillquip Tie Back connector to 10 3/4' casing and ran in hole from surface to 108 m." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk prior to pick/make up the 10 3/4' hanger. Performed same." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed elevator to 5½' DP elevator." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked/made up spear assy and connected same up to top drive. Drained the riser. String weight 12 MT." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with Tie Back string and set down 2 MT in Sub surface WH." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Made up Tie Back connection, turned the string 5 right hand turns. Applied 5000 ft/lbs to energize the metal seal. After 3 turns the spear released due to torque friction in Tie Back connector. Re-engaged spear and took over pull of 11 MT completed the 5 turns with final torque of 5000 ft/lbs. Verified space out by observing correct colour code through the surface WH B-annulus valve." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with the Spear assy. Racked back same in derrick." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box prior to rig down 10 3/4' casing handling equipment. Rigged down same." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box talk prior to RIH with Straddle cup tester. Made up and ran in with Straddle cup tester from surface to 138 m." "On 2008-01-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked/made up pump in sub and cement hose. Spaced out prior to test Tie-back connector 139 m." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Flushed cement line and pressure tested line to 50/345 bars 5/10 mins." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressure tested Tie-Back connector to 50/345 bars 10/10 mins. Volume pumped 82 litres bled off 80 litres. Observed no pressure building up in B-annulus." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Rigged down cement hose and pump in sub. POOH with Straddle cup tester from 139 m to surface. Hung up at 22 m. OOH with the Straddle cup tested. The lower cup tester had minor damaged. Changed out same. Laid out the Starddle cup test assy." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to making up the Adjustment sub setting tool." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked/made up the Adjustment sub setting tool. RIH from surface to 21 m. Took weight. Turned string 90º and passed obstruction. Continued RIH to 27.5 m." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Applied 140 bars to the Adjustment sub setting tool. Slowly pulled up to land in Latching ring groove and took over pull of 30 MT. String at ±27.1 m. Bled off the pressure in the string and kept the tension. Rotated the string at 2700 - 3000 Nm 17 turns. No travelling movement of the casing hanger. Observed through the B-annulus valve. When picked up the 30 MT over pull the casing hanger moved ± 2 cm up." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with Adjustment sub setting tool. Checked and function tested the Adjustment sub setting tool. No marks operated ok." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Changed out to back up Adjustment sub setting tool." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Evaluation meeting with onshore organisation. Meanwhile performed general maintenance on the rig floor." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH with the Adjustment sub setting tool." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Attempted to turn the Adjustment sub setting tool string using chain tongs. Made up TDS: RIH with Adjustment sub setting tool. Engaged the Adjustment sub setting tool in the vertical key slots. Turned string 10 turns to the right using the TDS, with 6000 Nm torque. Landed off the casing hanger, verified the Adjustment sub travel of 17 cm. By observation through B-annulus at WH. Released torque. Applied 140 bars to the Adjustment sub setting tool. Picked up 30 MT over pull, bled off the pressure. Turned the Adjustment sub setting tool 4 turns with 2 - 3 kNm, unable to engage the vertical key slots to torque up the casing hanger. Retracted the Adjustment sub setting tool. POOH with the Adjustment sub setting tool." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Evaluation meeting with onshore organisation. Meanwhile performed general maintenance on the rig floor." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 27m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with Adjustment sub setting tool. Applied 140 bars to the Adjustment sub setting tool. Took 10 MT over pull. Bled off the pressure. Ran back in 1cm, and pulled up slowly with 2 RPM rotation and engaged the vertical key slots. Applied 140 bars to the Adjustment sub setting tool. Took 30 MT over pull, bled off the pressure. Turned the string 1 turn to the right, and made up the casing hanger sleeve to 9500 Nm, total 11 turns. Retracted the Adjustment sub setting tool. POOH with the Adjustment sub setting tool." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Made up the Straddle cup tester. RIH and positioned the straddle cup tester across the Adjustment sub. Pressure tested same 20/345 bars 5/10 mins." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk prior to POOH with Straddle cup tester and lay out same. Performed same." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box prior to lay out Red Baron Spear assy. Performed same." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH and installed secondary Bowl protector at 20 m." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared the rig floor. Held tool box talk prior to pick/make up 9.567' drift." "On 2008-01-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked/made up 9.567' drift. RIH with 9.567' drift from surface to 45 m." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued RIH with 9.567' drift from 45 m to 150 m." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with 9.567' drift from 150 m to surface. Laid out the 9.567' drift." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to make/pick up GTV plug retrieving tool. Performed same." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed to power slips." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 630m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with the GTV plug retrieving tool from surface to 630 m." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 630m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made up to TDS and took up/down weight 93/88 MT neutral 91 MT. Rotated the string at 10 RPM with 2 kNm." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 635m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH and tagged plug at 635.4 m. Set down 12 MT picked up 20 MT over pull. Slacked off the neutral weight and turned the string ¼ turn to the left. Pulled up and the GTV plug retrieving tool had disengaged the GTV plug." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 625m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up and circulated down string with 200 lpm / 5 RPM / 1000 Nm, 0.5 m above the plug. Pulled out 2.5 m increased rate 1100 - 2400 lpm / 30 RPM. Washed out the Hi-vis pill over shakers." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 634m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with the GTV plug retrieving tool to engage the GTV plug at 635.4 m." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 641m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Latched GTV plug with LTCT retrieval tool according to BOT instructions. Released plug and allowed rubber element to relax for 15 mins prior to pulling plug." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: POOH with GTV plug from 641 m to 21 m MD on 5 1/2' DP. Removed PS-21 slips and installed masterbushing." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pulled LTCT head/GTV plug to surface. Observed nominal seat protector caught with GTV plug. Prepared for working on MS-seal setting tool." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Picked up 13 3/8' MS-seal setting tool. Attempted to dismantle/split tool - nogo. Laid down MS-seal setting tool." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up 13 3/8' seat protector running tool. RIH and installed nominal seat protector in surface wellhead at 20 m MD." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up 7' x 9 5/8' x 10 3/4' clean out string." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed from 5 1/2' to 3 1/2' handling gear. Picked up clean out assy #1 comprising of 7' scraper and magnet subs and hung off in rotary." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Cleared rigfloor. Prepared well control equipment." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 425m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.8 hours. Operational details: Held toolbox talk prior to picking up 3 1/2' singles. Ran 3 1/2' drillpipe to 425 m MD." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 425m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Made up kick joint with FOSV and tested same - ok." "On 2008-01-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 432m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Changed from 3 1/2' to 5' handling equipment. Picked up and made up clean out assy #2 comprising of X-over, PBR mill and liner top dress mill." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 443m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Picked up and made up clean out assy #3 comprising of 9 5/8' scraper, magnet, drift and x-over. Cleared rigfloor. Checked dies on PRS. Moved 2 ea damaged 5 1/2' drillpipe stands." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 893m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: RIH with clean out assemblies on 5' DP from 443 m to 893 m MD." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 893m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Performed toolbox talk / handover meeting with new drilling crew." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1800m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: Continued to RIH with clean out assemblies on 5' DP from 893 m to 1800 m MD." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1885m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: RIH with clean out assemblies from 1800 m to 1885 m MD. Picked up and made up clean out assy#4 comprising of 10 3/4' scraper, magnet and x-over to 5 1/2' DP." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1930m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with clean out assemblies from 1885 m to 1930 m MD on 5 1/2' DP." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1930m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Checked tugger lines and FWD PRS due to high winds in the range of 50-60 knots." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2290m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Continued to RIH with clean out assemblies from 1930 m to 2290 m MD on 5 1/2' DP. Observed dropped object from FWD PRS vertical hose bundel. Halted operation for further investigation." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2290m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Investigated situation. Found 3 ea hose bundle securing pins dropped to rigfloor. Each pin approx 20 cm / 220 grammes. Halted operation as it was impossible to repair the damage due to high winds." "On 2008-01-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2290m. The activity was categorized as 'interruption -- other' and lasted for 14.2 hours. Operational details: Waiting on improved weather conditions to perform repair on FWD PRS. Wind speed 60 knots. Meanwhile : -Performed general maintenance on aft IR -Performed general housekeeping and cleaning in moonpool, rigfloor, shakers and pitroom -Put protectors on pin end of 7' tubing laid out on deck" "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Waiting on improved weather conditions to perform repair on FWD PRS. Wind speed 60-70 knots. Meanwhile : -Performed general housekeeping -Secured drillstring and parked TDS for maintenance -Injected slop in F-12 annulus -Prepared spare parts and tools for performing PRS repair -Inspected and tested completion assemblies" "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 6.5 hours. Operational details: Waitied on improved weather conditions to perform inspection and repair of FWD PRS. Meanwhile : -Performed general cleaning in moonpool, pitroom and shakers -Injected slop/overflush in F-12 annulus. Insufficient overflush due to exceeded pressure limit." "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2334m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Performed derrick inspection after high winds." "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Inspected FWD PRS. Dragchain and hoses were severly twisted and partly torn down. Assessed situation and found damage to severe for immediate repair. Prepared for making repairs on AFT PRS instead." "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to using work basket." "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Inspected FWD PRS dragchain for loose items, removed and secured accordingly." "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Brought scaffolding material to drillfloor and prepared for buliding scaffolding in derrick. Found that scaffolding job could not commence due to high winds and working hours regulations." "On 2008-01-05, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Waited on improved weather condtions and/or qualified rest for scaffolding crew. Meanwhile : -Changed oil cooler on TDS -Performed general cleaning in moonpool, pitroom and shakers" "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Waited on qualified rest for scaffolding crew. Meanwhile : -Changed oil cooler on TDS -Brought scaffolding material to derrick -Emptied skimmer tank -Made measurements for spare parts on FWD PRS -Checked and measured completion assemblies" "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Seafastened AFT PRS." "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 9.2 hours. Operational details: Held toolbox talk prior to building scaffolding around AFT PRS. Built scaffolding. Prepared security net for installation underneath AFT PRS working area." "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Held toolbox talk. Installed canvas around scaffolding. Prepared for installing security net. Had to abort manriding operations due to maintenance of Siemens system and risk of main power loss." "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Performed upgrade of Siemens system. Meanwhile continued to install canvas around scaffolding. Prepared lights for installation on scaffolding work platform." "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Installed security net around AFT PRS scaffolding platform. Transferred tools and equipment to derrrick." "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Mechanics worked on AFT PRS." "On 2008-01-06, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Held toolbox talk. Rigged down security net due to wrong allignment/position of PRS relative to scaffolding platform." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Waited on qualified rest for scaffolding crews. Meanwhile : -Continued rigging down security net -Performed service on TDS -Tested MS-seal setting tool -General houskeeipng in drilling areas" "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Prepared for removing scaffolding around AFT PRS." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Removed part of scaffolding around AFT PRS." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Turned AFT PRS 180 deg for better access to upper drive / shaft." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Installed security net underneath AFT PRS." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Rebuilt scaffolding around AFT PRS. Meanwhile laid out TCP guns on top of tubing in STB AFT bay." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Performed repair work on AFT PRS upper drive. Meanwhile tested Siemens/ESD system." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Not able to do effective/continuous repair of AFT PRS due to interruptions in power supply from ongoing test of Siemens/ESD system." "On 2008-01-07, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Finished testing of Siemens/ESD system. Worked on AFT PRS upper drive." "On 2008-01-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Performed repair work on AFT PRS upper drive. Meanwhile removed cantilever hatch and prepared for lifting Xmas tree from transport basket to moonpool." "On 2008-01-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Function pipe rams and HCR's on BOP - ok. Function tested annular preventer - closing time 42 sec versus requirement of 30 s. Meanwhile performed repair work on AFT PRS upper drive." "On 2008-01-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Performed repair work on AFT PRS upper drive. Meanwhile : -Lifted Xmas tree from moonpool -Prepared hose from moonpool to wellhead -Laid out 7' pup joints" "On 2008-01-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 13.0 hours. Operational details: Performed repair work on AFT PRS upper drive Meanwhile : -Cleaned cameras in derrick -Worked on dragchain for crane in moonpool -Tested new V-ICIS software for mudpumps -Reset V-ICIS control system after power shut down -Prepared subsea caps for wellheads/conductor" "On 2008-01-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Performed repair work on AFT PRS upper drive. Halted repair work due to high winds above set limitations for working in heights. Winds > 40 knots." "On 2008-01-08, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Waited for weather condtions to improve for resuming AFT PRS repair work. Meanwhile : -Lifted subseas caps from main deck to Centralizer deck -ROV closed valve on DCI hose for pressure testing" "On 2008-01-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Waited for weather condtions to improve for resuming AFT PRS repair work. Meanwhile : -Blinded pop off and tested DCI hose using cement unit to 200 bar / 10 min - ok -ROV opened valve on DCI hose -Installed debris caps on F-5, F-14 and F-15 wellheads -Removed temporary cap and installed debris cap on F-1 conductor -Attempted to inject slop in F-12 annulus. Pressure bulit up rapildly, 190 bar at approx 1 m3 pumped -Operated/functioned annular preventer to gain faster closing time" "On 2008-01-09, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 18.0 hours. Operational details: Waited for weather condtions to improve for resuming AFT PRS repair work. Meanwhile : -Removed lead target in cement unit test line -Performed general maintenance in drilling areas -Cleaned pits Winds : 12:00 81 knots 14:00 61 knots 16:00 56 knots 18:00 70 knots 20:00 53 knots 22:00 64 knots" "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Waited for weather condtions to improve for resuming AFT PRS repair work. Meanwhile : -Performed maintenance on BX elevators -Function tested annular preventer, 28 seconds to close (determined from readback pressure) -Drained mainfold line to wellhead -Performed derrick inspection prior to resume work on AFT PRS -Inspected scaffolding in derrick Winds : 24:00 53 knots 02:00 40 knots" "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Performed derrick inspect after period of high winds. Inspected scaffolding work platform." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Waited for weather condtions to improve for resuming AFT PRS repair work. Winds : 04:00 40 knots 06:00 39 knots" "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Performed crown block inspection prior to accessing scaffolding platform for continued repair." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 9.8 hours. Operational details: Continued working on AFT PRS upper drive. Meanwhile : -Assisted in repairing AFT PRS -Cleaned pits -Functioned flowline isolation valve wih 1450 psi -Function tested AFT PRS" "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to remvoing scaffolding." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed tools and equipment from AFT PRS scaffolding platform." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Assissted scaffolding crews in removing scaffolding from derrick." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting for continuation of removing scaffolding." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2335m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Waited on weather conditions to improve for continuing removing scaffolding." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Waited on weather condictons to improve. Wind speed 56 knots." "On 2008-01-10, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Checked FWD PRS for losse items. Secured FWD PRS by wrapping damaged parts with security net." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Continued to secure FWD PRS." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing scaffolding from derrick." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Removed scaffolding from derrick." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Calibrated block height after ESD power shut down." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Calibrated crown block. Re-set I-VICIS software for rig equipment after power shut down(s)." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2235m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to installing PS-21 automatic slips and RIH. Installed PS-21." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2376m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH with clean out assemblies on 5 1/2' DP from 2235 m to 2376 m MD." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2407m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Made up TDS to cleaning string. Scraped and cleaned FLX packer area from 500 m to 520 m MD with 10 3/4' scraper. Pumped 80 m3 contamianted brine at 2500 lpm while reciprocating and rotating pipe at 60 RPM. Max torque 9 kNm. Up/down weights 146/117 MT." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2578m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH with clean out assemblies on 5 1/2' DP from 2407 m to 2578 m MD. Could not release PS-21 slips after connection." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2578m. The activity was categorized as 'interruption -- other' and lasted for 5.2 hours. Operational details: Repaired on PS-21 slips. Released slips. Exchanged PS-21 with PS-30 slips." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: RIH with scraper assemblies from 2578 m to 3080 m MD." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3107m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Made up TDS to cleaning string. Scraped and cleaned gun hanger area from 3080 m to 3100 m MD with 7' scraper. Pumped SW at 1500 lpm while reciprocating and rotating pipe at 60 RPM. Max torque 17 kNm. Up/down weights 144/125 MT. Made connection and observed U-tube from well due to overweight brine pumped at an earlier stage. Scraped and cleaned area from 3100 m to 3105 m MD. Total volume pumped approx 30 m3." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3425m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: RIH with scraper assemblies from 3107 m to 3425 m mD." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3442m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up TDS to cleaning string. Scraped and cleaned production packer setting area from 2980 m to 3000 m MD with 9 5/8' scraper. Pumped 30 m3 of SW at 1500 lpm while reciprocating and rotating pipe at 60 RPM." "On 2008-01-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3458m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Recorded parameters while circulating and rotating : Flow 1100 lpm / 50 RPM / Up weight 167 MT / Down weight 145 MT / Torque 25 kNm / SPP 72 bar. Took Up/down weight without circulation and rotation : Up weight 190 / Down weight 134 MT. Set torque limit to 27 kNm. RIH while circualting at 1100 LPM and rotating 50 RPM. Tagged top of PBR at 3026,2 m MD (bit depth 3457,9 m MD). String stalled out due to excessive torque, relaxed weight to regain rotation, which fluctuated between 20-50 RPM. Picked up above PBR. Ran back in to 3026 m (bit depth 3457,7 m MD) and dressed PBR for 1 min. Max torque 27 kNm." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3453m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Picked string 5 m above PBR and marked pipe for lowest reciprocation depth." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3453m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to displacing well from treated SW to 1,03 packer fluid." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3453m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Added Oxygen scavenger and prepared for displacement." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3453m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Pumped 20 m3 hivis Soap pill followed by 20 m3 TSW spacer and 245 m3 1,03 sg packer fluid. Reciprocated and rotated pipe with 50 RPM. Pump rate 3300-3500 lpm. SPP 214-234 bar. Sampled returns and made consecutive NTU readings : 780/485/388/340/>1000/477/387/339/303 NTU." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3453m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke off and set back 1 stand of 5 1/2' DP. Observed U-tube from annulus to pipe." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3453m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Mixed more 1,03 sg packer fluid for filling well when POOH. Meanwhile observed well." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3453m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Emptied SW from trip tanks. Filled triptanks. Topped up welll with 1,2 m3 packer fluid." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3216m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: POOH with cleaning assemblies from 3453 m to 3216 m MD on 5 1/2' DP." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: POOH with cleaning assemblies from 3216 m to 2175 m MD." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to moving PS-30 automatic slips." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed PS-30 automatic slips and inserted masterbushing. Conducted kick drill. Secured well prior to ESD testing." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed swedge on TDS for pressure testing IBOP." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pressure testing TDS and manifold." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Tested upper/lower IBOP to 30/345 bar 5/10 min. Progress intrerrupted by ESD testing." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Waited on ongoing Siemens/ESD testing. Meanwhile tested standpipe manifold valves to 30/345 bar 5/10 min." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Got power shut down on rig. Waited on ongoing Siemens/ESD testing. Meanwhile removed scaffolding, cleaned and tidied in wellhead module." "On 2008-01-12, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Re-set V-ICIS-system. Calibrated block. Meanwhile tested valves in standpipe manifold to 30/345 bar 5/10 min. Cleaned and tidied in wellhead module." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2175m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Broke off swedge on TDS. Held toolbox talk prior to continue pulling cleaning string." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1870m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: POOH with cleaning assemblies on 5 1/2' DP from 2175 m to 1870 m MD. Used manual slips." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1870m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Held toolbox talk. Removed bowl and masterbushing. Inserted PS-30 slips dressed for 5' drillpipe. Attempted to run HTS to drillfloor, no-go due to lack of calibration. Broke out and laid down cleaning assy #4 with 10 3/4' scraper/magnet on deck. Observed swarf on magnet. Broke out singel and laid down on drillfloor." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1870m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Calibrated HTS after ESD shut down." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 735m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: POOH with cleaning assemblies on 5' DP from 1870 m to 735 m MD." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 440m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: POOH with cleaning assemblies on 5 1/2' DP from 735 m to 440 m MD." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 440m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing PS-30 slips. Observed falling object from derrick when attempting to lift out slips. Shackle and tag fell down on drillers cabin and deflected to drillfloor. Halted operation for investigation and derrick inspection." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 440m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Inspectred crown and TDS. Found source of shackle and tag to be from swivel between chain and wire on tugger." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 440m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed PS-30 slips from rotary and inserted master bushing." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 417m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Racked back last stand and 5' drillpipe. Laid out 9 5/8' scraper assy and 7' top dress/polish mill. Observed swarf on magnet. Inspected top dress mill - ok. Found piece of metal jammed in polish mill." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 417m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Held toolbox talk prior to changing handling gear. Changed from 5' to 3 1/2' handing equipment. Inserted PS-21 dressed for 3 1/2' pipe in rotary." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 10m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 5.2 hours. Operational details: POOH with cleaning assembly on 3 1/2' DP. Broke out and laid down 3 1/2' singles. Had problems to unlatch from pipe due to overgauge pipe close to couplings." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Laid out 7' scraper assembly." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Held toolbox talk. Picked up Vetco bowl protector retrieval tool and RIH with same. Closed annular and flushed choke and kill line and manifolds from SW to 1,03 packer fluid at 1500 lpm." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with retrieval tool and latched bowl protector at 20,1 m MD. POOH with tool and racked back stand." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to setting 10 3/4' MS-seal." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Made up seal assembly to running tool. Made up control lines to running tools." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Ran MS-seal running tool and strapped control line to pipe. Landed MS seal over 10 3/4' hanger at 20,8 m MD. Pressured up lock ring energizing line to 1500 psi and locked tool to WH. Took 7 MT overpull and verified tool set. Pressured up thorugh MS seal setting line to 4300 psi. Observed movement of string. Bled off pressure on control lines." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressure tested MS seal through test ports 3 and 4 on wellhead to 345 bar/10 min - ok." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released MS setting tool with 5 turns clockwise rotations. POOH with MS seal setting tool. Laid out tool and cleared rigfloor." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held toolbox talk prior to leak testing surface tie back. Emptied SW on cement unit and filled tanks with drillwater. Verified B-annulus valves and test ports open. Lined up from cement unit to pump in kill line on BOP underneath shear ram. Pressurised line to 10 bar and opened HCR on BOP to verify line up. Closed shear ram." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Performed low pressure test of surface tie-back to 30 bar. Pressure dropped from 30,8 bar to 30,6 bar over 5 min - ok. Volume pumped 245 liter. Pressured up from 30 bar to 345 bar at 200 lpm. Total volume pumped 2408 liter. Observed pressure decline from 345 to 312 bar over 10 mimutes indicating a leakage rate of 21 l/min. Observed annulus which continued to flow after pressurising finished. Checked for leaks accross HCRs and shear ram - none observed. No increase in trip tank. Bled back pressure to zero. Recovered 2058 liter bled back volume. Checked pressure curve and found possible/neglible deflection around 300 bar." "On 2008-01-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Discussed situation. Meanwhile leak tested surface line to BOP to 345 bar / 10 min - ok." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Discussed situation. Decided to do pressure test in steps to identify the onset of the leakage. Fitted B-annulus with pressure gauge." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pressured up well in 50 bar increments: 50 bar / 415 liter - Presssure drop 0,97 bar / 5 min 100 bar / 775 liter - Pressure drop 0,8 bar / 5 min 150 bar / 1099 liter - Pressure drop 1,8 bar / 5 min 200 bar / 1451 liter - Pressure drop 5,3 bar / 5 min corresponding to a leakage rate of 7 l/min." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed B-annulus valves. Observed wrong placement of pressure gauge and unsuited scale on same. Bled back pressure to 150 bar. Changed pressure gauge. Pressure dropped from 150 bar to 142 bar over 30 min (1,8 l/min) while working on annulus. When opening inner B-annulus valve a pressure of 12 bar could be observed on the pressure gauge immediately." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressured up well to 200 bar and observed annulus pressure increase to 25 bar. Pressure fell on well and increased on annulus : 5 min : well; 2,4 bar drop / annulus; 3 bar cummulative increase 10 min : well; 4,6 bar drop / annulus; 6 bar cummulative increase 15 min : well; 6,4 bar drop / annulus; 9 bar cummulative increase 20 min : well; 7,5 bar drop / annulus; 11 bar cummulative increase Indication of leakage from tie-back casing to B-annulus confirmed. Leakage rate with closed annulus at approx 200 bar - 2,5 l/min." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Bled back pressure on casing and B-annulus." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared for testing BOP. Picked up BOP test plug and RIH with same. Set test plug in surface wellhead." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: Tested 18 3/4' surface BOP according to Mærsk procedure." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.5 hours. Operational details: Tested 18 3/4' surface BOP." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: POOH with BOP test plug and laid down same." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Discussed further actions with town. Meanwhile picked up and made up 10 3/4' cup tester." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to RIH with 10 3/4' cup tester." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 10 3/4' cup tester on 5 1/2' DP to 30,5 m MD. Closed UPR and verified lineup." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressure tested ASH and casing hanger against 10 3/4' cup tester. Stepped up pressure in 50 bar increments from 100 bar and held each step for 5 min. Obtained good test at 345 bar. Pumped and bled back 79 l." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 132m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 10 3/4' cup tester on 5 1/2' DP from 30,5 m to 132 m MD. Closed UPR." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 132m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressure tested upper tie-back string against 10 3/4' cup tester. Stepped up pressure in 50 bar increments from 100 bar and held each step for 5 min. Obtained good test at to 345 bar. Pumped and bled back 172 liter." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with 10 3/4' cup tester on 5 1/2' DP from 132 m to 150 m MD. Closed UPR." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pressure tested tie-back adaptor against 10 3/4' cup tester. Stepped up pressure in 50 bar increments from 100 bar and held each step for 5 min. Obtained good tests at 345 bar. Entire upper tie-back string tested to 345 bar / 10 min - ok. Pumped and bled back 183 liter." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with 10 3/4' cup tester on 5 1/2' DP. Broke out and laid down cup tester." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed shear rams and performed fingerprinting of trip tank : Added 20 l water above shear ram. Observed 20 l increase (driller/logger) Added 10 l water above shear ram. Observed 10 l increase (driller/logger)" "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Lined up to pump down well and re-test the complete tie-back string." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Pressured up well to 101 bar at 100 lpm. Pumped 712 liter. Dropped from 101,6 bar to 100,7 bar in 5 min - ok. Pressured further up to 200 bar at 100 lpm. Total pumped 1410 liter. Dropped from 200 bar to 195,6 bar in 5 min. Leaking at approx 6 l/min. Pressured further up to 250 bar. Total pumped 1806 liter. Pressure drop 4 bar/5min. Pressured further up to 300 bar. Total pumped 2184 liter. Pressure drop 4 bar/5 min. Measured leakage rate of 4 l/min on B-annulus. Pressured further up to 346 bar. Pressure drop 0,5 bar/min. Measured leakage rate of 4 l/min on B-annulus." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Pressured up well to 345 bar every 15 min. Pressure dropped 0,5 bar/min. Measured a steady leakage rate of 4 l/min on B-annulus. Observed increase in leakage rate of approx 12 l/min each time the well was pressurised back to 345 bar. No significant change in leakage rates could be observed. Bled off pressure on well." "On 2008-01-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Picked up and RIH with nominal bowl protector at 20,8 m MD. Set bowl protector and pulled stand." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Waited for RTTS to arrive with supply boat. Meanwhile : -Worked on IR -Serviced manrider winches -Changed centralizers for F-12 riser on Centralizer deck and tensioning deck -Functioned flow line valve" "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up 1 stand of 5 1/2' DP to put underneath 9 5/8' RTTS packer. Received RTTS, checked and measured same." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Made up 9 5/8' RTTS packer." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2350m. The activity was categorized as 'drilling -- casing' and lasted for 5.8 hours. Operational details: RIH with 9 5/8' RTTS packer on 5 1/2' DP from 45 m to 2350 m MD." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2352m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set 9 5/8' RTTS by righthand rotation and set down 3 MT. Packer element set +/- 50 m above 9 5/8' seal stinger." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2352m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up to pump from cement unit down kill line on BOP. Closed pipe ram, verified line up. Pressure tested 9 5/8' x 10 3/4' tie-back stinger above the RTTS packer to 345 bar / 10 min - ok. Volume pumped/bled back 1330 liter. No returns observed on B-annulus." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2352m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Opened pipe ram. Released 9 5/8' RTTS packer. RIH from 2352 m to 2420 m MD. Struggled to pass PBR pocket with end of pipe at 2400 m MD. Picked up and slacked off several times and passed pocket." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2421m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set 9 5/8' RTTS packer by righthand rotation and set down 3 MT. Packer element set +/-20 m into 9 5/8' liner." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2421m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to pump from cement unit down TDS and DP. Verified line up. Pressure tested 9 5/8' x 7 ' liner below the RTTS packer to 345 bar / 10 min - ok. Volume pumped/bled back 1100 liter." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2421m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up to pump from cement unit down kill line on BOP. Closed pipe ram, verified line up. Pressured up to 170 bar in stepwise manner : 30 bar / 10 min - ok. Cumulative pumped 145 liter 100 bar / 5 min - ok. Cumulative pumped 400 liter 171,5 bar. Cumulative pumped 712 liter - dropped 3 bar / 5 min. Leakage rate 2 l/min. Onset of leak from B-annulus could be observed at 165 bar." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2420m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Allowed pressure to bleed off in attempt to establish leakage free pressure : 160 bar - dropped 5,1 bar / 10 min (3,2%) - leakage 1,5 l/min 150 bar - dropped 4,6 bar / 10 min (3,1%) - leakage 1,5 l/min 140 bar - dropped 3,6 bar / 10 min (2,5%) - leakage 1,1 l/min 130 bar - dropped 3,2 bar / 10 min (2,5%) - leakage 1,0 l/min 120 bar - dropped 2,4 bar / 10 min (2,0%) - leakage 0,8 l/min 110 bar - dropped 2,4 bar / 10 min (2,2%) - leakage 0,7 l/min 100 bar - dropped 2,6 bar / 10 min (2,6%) - leakage 0,9 l/min 90 bar - dropped 1,7 bar / 10 min (1,9%) - leakage 0,5 l/min 80 bar - dropped 1,9 bar / 10 min (2,4%) - leakage 0,7 l/min 70 bar - dropped 1,5 bar / 10 min (2,2%) - leakage 0,5 l/min Bled pressure in well to zero." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2420m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released 9 5/8' RTTS packer with 24 MT overpull according to Halliburton instructions. Allowed packer element to retract." "On 2008-01-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2180m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with 9 5/8' RTTS packer on 5 1/2' DP from 2420 m to 2180 MD. Pulled carefully through PBR pocket - no addtional drag observed." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Continued to POOH with 9 5/8' RTTS packer on 5 1/2' DP from 2180 m to 40 m MD." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke out an laid down 9 5/8' RTTS packer. Racked back last stand." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Waited for plan of action from town. Meanwhile did routine testing of FOSV's and Gray valve." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Waited for plan of action from town. Meanwhile did routine testing of FOSV's and Gray valve." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 9.5 hours. Operational details: Waited for instuctions from town. Meanwhile : -Pressure tested safety valves -Performed manitenance on rotary table lock -Performed general housekeeping and PM's on drillfloor -Removed BOP carrier from BOP" "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: Recieved instruction from town to run guns. Waited on weather due to high winds, cranes down. Meanwhile rigged up casing tong, dressed PS-21 slips for 4 1/2' and dressed BX elevator with 5' inserts." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Laid out 4 1/2 perforation guns, firing heads and MAXR anchor on top of tubing in STB AFT bay. Made up FOSV with x-overs to perforation guns." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Held pre-job meeting on drillfloor. Made up Gray valve to stand of 5 1/2' DP and racked back." "On 2008-01-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 38m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Ran in hole with 4 1/2' Orient exact weights/perforation guns from surface to 38 m MD." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 195m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Ran in hole with 4 1/2' Orient exact weights/spacers/perforation guns from 38 m MD to 195 m MD." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 195m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Removed PS-21 slips from rotary and inserted masterbushing and bowl. Removed and set back Odfjell casing tong. Took up weight 78 MT." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 200m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Picked up and made up E-fire firing head. Made up firing head to swivel on top of gun section. Hung off in 3 1/2' collar slips and secured with dog collar." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 206m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Picked up and made up Pro-fire firing head. Made up firing head. Hung off in 3 1/2' collar slips and secured with dog collar." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 218m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Lifted in MAXR assembly complete with setting tool. Made up 3 1/2' pup joint and X-over to assembly while laying on HTS. Picked up assembly and made up to Pro fire firing head. Checked adjustment of MAXR setting sleeve, removed transport studs and fitted shear pins. Hung off in 3 1/2' DP slips." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 252m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with 4 1/2' Orient exact perforation gun assy on 3 1/2' DP from 217 m to 252 m MD according to tally." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 294m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: RIH with 4 1/2' Orient exact perforation gun assy on 3 1/2' DP from 252 m to 294 m MD according to tally. MU PBR no-go locator sub." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 294m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Held tool box meeting and changed to 5' handling equipment." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 862m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: RIH with 4 1/2' Orient exact perforation gun assy on 5' DP from 294 m to 862 m MD according to tally." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 862m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Stopped RIH. Discussed testing requirements and further plans for F-12 with town." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 300m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: POOH with 4 1/2' Orient exact perforation gun assy on 5' DP from 862 m to 300 m MD according to tally." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 300m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Held tool box meeting and changed to 3 1/2' handling equipment." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 217m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: POOH with 4 1/2' Orient exact perforation gun assy on 3 1/2' DP from 300 m to 217 m MD according to tally." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.8 hours. Operational details: Held tool box talk prior to handling guns on rig floor. POOH with 4 1/2' Orient exact perforation gun assy from 217 m to OOH." "On 2008-01-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Flushed lines and pressure tested from pump room to lower kill on BOP 35/240 bar for 5 min." "On 2008-01-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Flushed lines and pressure tested from cement unit to outer manual valve on B-annulus 35/250 bar for 5 min. Meanwhile performed maintenance on TDS and rig floor equipment." "On 2008-01-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Waited for plan of action from town. Meanwhile performed maintenance on TDS and rig floor equipment." "On 2008-01-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 16.0 hours. Operational details: Waited for plan of action from town. Meanwhile : -Performed 6 month maintenance on TDS -Installed centralizer ring on F-7 -Transfered 7 m3 packer fluid from pit 3 to cmt unit with MP2 -Installed back up BX elevator and function tested same -Disconnected winch on aft TDS working platform" "On 2008-01-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed in-between test to 220 bar / 10 min on multibowl BT-seals." "On 2008-01-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather due to high winds up to 87 knop and danger for people to be present in well head module." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on weather due to high winds up to 72 knop and danger for people to be present in well head module." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- well control' and lasted for 2.2 hours. Operational details: Waited on weather due to high winds up to 60 knop and danger for people to be present in well head module. Meanwhile inspected AFT PRS and found damage on drag chain. Barried off rig floor." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk for testing 10 3/4' x 14' annulus. Performed line test to 20 bar to verify correct line up. Closed shear ram." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Adjusted geoservices logging screen for documentation of test" "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pressured up to 35 bar on B-annulus. Pressured up to 175 bar with MP2 using packer fluid on csg side. Observed 17 bar pressure increase on B-annulus due to ballooning (35-52 bar) Attempted to pressure up B-annulus to 220 bar with cmt unit. Stopped pumping at 97 bar and only 16 ltrs pumped (theoretical volume to 97 bar = 280 ltr)." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Bled off B-annulus and csg to 0 bar and investigated surface lines. Disconnected 5K hose from cmt unit to surface wellhead and flushed through to verify no restrictions. Reconnected 5K hose to B-annulus and performed new line test 30/225 bar 5/10 min against closed outer valve on wellhead outlet. Pressured up to 50 bar on B-annulus with only 23 ltr pumped (23 ltr corresponds to pressuring up volume down to subsea wellhead, indicating blockage in 10 3/4' hanger annulus ports)." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Bled off pressure on B-annulus and had time-out to evaluate further action." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk for testing 10 3/4' x 14' annulus. Performed line test to 20 bar to verify correct line up for both BOP kill line and B-annulus. Pressured up csg with MP2 to 50 bar/400 ltrs - Recorded 10 bar on B-annulus from cement unit. Pressured up csg with MP2 to 70 bar/155 ltrs - Recorded 12,4 bar on B-annulus from cement unit. Pressured up csg with MP2 to 156 bar/644 ltrs - Recorded 21 bar on B-annulus from cement unit. Observed leak into B-annulus at 156 bar, confirming communication through annulus ports in 10 3/4' hanger from below (recorded pressure increase above ballooning effect). Recorded 1,9 bar/10min pressure increase on B-annulus with 135 bar differential pressure." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Had time-out to evaluate further action. Made arrangements for punching holes in 9 5/8' csg. Meanwhile logged pressure on csg and B-annulus. Recorded 0,25 bar/10min pressure increase on B-annulus with 56 bar differential pressure." "On 2008-01-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Waited for tubing puncher equipment and schlumberger personnel to arrive on the rig. Bled off pressure on B-annulus from 60 to 2 bar in preparation to test shear rams. Observed pressure on csg driopping from 116 bar to 106.4 bar while bleeding off on B-annulus (due to balloning effect). RIH with WBRT and pulled WB. RIH with 2 stds of 5' DP and test plug to 100 m MD. Sat test plug." "On 2008-01-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Waited for tubing puncher equipment and schlumberger personnel to arrive on the rig. Tested shear rams 20/345 bar 10 min with packer fluid, 82 ltrs pumped and 78 ltrs in return. POOH with test plug and LO same. RIH with WB and sat same." "On 2008-01-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 10.0 hours. Operational details: Waited for tubing puncher equipment and schlumberger personnel to arrive on the rig. Meanwhile: -Performed derrick inspection after high winds -Changed out encoder, replaced bended link on drag chain and calibrated AFT PRS. -Cleared future equipment room. -Performed maintenace on crew conveyer between CRI and STB transport conveyer -Cleared rig floor prior to running WL." "On 2008-01-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: Placed wireline units on cantiliver and port leg and hooked them up electrically. RU umbilical from Schlumberger logging unit to Seawell wireline winch. Installed add-on drum with 7/16' cable." "On 2008-01-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Prepared and loaded 1 11/16' HNS Puncher. Changed to Schlumberger collector. MU MH-22 logging head for 7/16' cable. RU sheave wheels on rig floor." "On 2008-01-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 8.5 hours. Operational details: Continued RU wireline equipment and troubleshot power supply for wireline winch. Modified depth system on wireline winch drum. Function tested CCL tool." "On 2008-01-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2450m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: MU and RIH with toolstring to 2450 m. Correlated depth to tally using CCL and fired 1 11/16' HNS Puncher at 2395-2392 m MD." "On 2008-01-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH with toolstring and LO gun assembly. Confirmed all 41 shots were fired." "On 2008-01-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held pre job meeting with involved personnel. Lined up cement unit to pump down casing. Disconnected hose on B-annulus and observed flow due to U-tubing effect. Pumped down casing 300 lpm and observed full communication via holes punched in 9 5/8' csg." "On 2008-01-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Hooked hose back up on B-annulus and performed a line test 35/220 bar 5/10 min. Bled off pressure to 20 bar, opened B-annulus valve and verified line-up. Lined up to monitor B-annulus on standpipe. Pressured B-annulus through punched holes in 9 5/8' x 10 3/4' tieback string to 220 bar / 10 min using 2196 ltrs drillwater from cement unit. Had 2.6 bar drop in 10 min." "On 2008-01-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Ivestigated leak by performing line tests against various valves. Isolated standpipe by closing valves on B-annulus wellhead. Unable to obtain pressure test within 1% pressure drop. Opened B-annulus valves and bled off pressure through stanpipe and into trip tank. Re-arranged line-up." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Re-tested B-annulus through punched holes in 9 5/8' x 10 3/4' tieback string to 220 bar / 10 min using packer fluid from cement unit. Observed 2.2 bar drop in 10 min. Pumped 2087 ltrs and bled back 1980 ltrs. Both manual valves on wellhead B-annulus had been tested to 220 bar/10 min during line tests." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RU for running TCP guns. Prepared firing heads and loaded batteries." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box meeting for RU and RIH with TCP guns. Meanwhile closed shear rams due to slow increase in trip tank of 150 ltrs/hr." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Investigated increase in trip tank. No pressure build up recorded. Observed well on trip tank. No gain observed." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 27m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: MU TCP guns and lowered each section into hole by BX elevators from surface to 54 m MD." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 173m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: MU 4 1/2' TCP guns and lowered each section into hole by BX elevators from surface to 173 m MD." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: POOH and LO 4 1/2' gun assembly from 173 to 48 m. Held last 9 joints standby in TDS." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Held tool box talk. Greased up valves and pressure tested kill manifold to 345 bar/10 min." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Performed two line tests to 345 bar/10 min. Tested B-annulus through punched holes in 9 5/8' x 10 3/4' tieback string against outer manual valve on B-annulus to 220 bar / 10 min using packer fluid from cement unit. Observed 0 bar drop in 10 min. Pumped 2193 ltrs and bled back 2200 ltrs." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed K-3 valve on on kill manifold and bleed off pressure down to cmt unit. Lined up cmt unit to B-annulus through hose from moonpool. Closed inner manual valve on B-annulus and equalized and opened outer valve. Bled off pressure on cmt unit down to 10 bar. Inflow tested inner manual valve on wellhead B-annulus to 220 bar/10 min. Bled off all pressures." "On 2008-01-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 292m. The activity was categorized as 'completion -- perforate' and lasted for 7.2 hours. Operational details: MU 4 1/2' TCP guns and lowered each section into hole by BX elevators from surface to 173 m MD. MU orient exact weight spacers from 173 m to 195 m MD. MU eFire firing head assembly and ProFire firing head assembly. MU MAXR assembly onto the HPA fill-sub assembly and RIH with TCP guns on 3 1/2' DP from 217 to 285,5 m MD. MU PBR no-go locator sub." "On 2008-01-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1311m. The activity was categorized as 'completion -- perforate' and lasted for 5.2 hours. Operational details: RIH with 4 1/2' TCP guns on 5 1/2' DP to 1311 m MD." "On 2008-01-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1311m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Had VFD-fault (electrical problem) on AFT PRS racking arm." "On 2008-01-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1311m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: The upper racking arm on the AFT PRS could not move because brakes were locked. Meanwhile installed TIW on string and function tested BOP at low pressure." "On 2008-01-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3310m. The activity was categorized as 'completion -- perforate' and lasted for 11.5 hours. Operational details: Removed TIW and installed XO to 5 1/2' DP. Changed handling equipment to 5 1/2'. RIH with 4 1/2' TCP guns on 5 1/2' DP from 1311 m to 3310 m MD. Up weight 212 MT / down weight 129 MT." "On 2008-01-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3316m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Tagged TOL at 3315.7 m MD and landed no-go locator on top of PBR. Sat down 5 MT. Pulled to up-weight and marked the string ( 1.9 m stretch in string). Reciprocated string 10 times to orientate the guns. Tagged TOL again at 3315.6 m and landed no-go locator on top PBR. Sat down 5 MT. Pulled to up-weight and verified mark on string. PO 9 m with 4 1/2' TCP guns to locate top shot at 3130 m MD. Slacked off weight by releasing 0.5 m stretch in string. Held tool box meeting before pressuring up the well when reciprocating string." "On 2008-01-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3305m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Checked line-up. Broke circulation by pumping 300 lpm at 5 bar. Closed annular BOP. Pressured up annulus and DP simultaniously by pumping 800 lpm to 220 bar to activate MAXR setting tool. Held pressure for 2 min. Bled off pressure and verified that pressure was zero before opening annular BOP. Pumped 3100 ltrs and bled back 3000 l. One cycle used on ProFire. Waited 25 min, from activation, for MAXR to set. Sat down 2 MT to confirm that MAXR had been sat. Picked up 3 m and re-checked up/down weights to confirm that the hanger had been released from the running tool. String weight was reduced by 14 MT." "On 2008-01-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1802m. The activity was categorized as 'completion -- perforate' and lasted for 4.5 hours. Operational details: POOH with MAXR setting tool on 5 1/2' DP from 3305 to 1802 m MD." "On 2008-01-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 8.8 hours. Operational details: POOH with MAXR setting tool on 5 1/2' DP from 1802 m to OOH. LO gun hanger setting tool and RD handling equipment." "On 2008-01-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: RIH and pulled secondary bowl protector in surface wellhead at 20 m MD. MU jet sub and cleaned BOP and wellhead at 2000 lpm / 8 bar / 10 RPM. LO same." "On 2008-01-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 4.0 hours. Operational details: MU kick assembly. RU csg tong and prepared to run 7' tubing. Lifted in place BOT and WellDynamics' cable drums. Installed FMS." "On 2008-01-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 73m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: Held pre-job meeting with involved personnel. MU and ran 7 1/2' seal stem (no seals) with ratcheting muleshoe assembly. Function tested ratcheting muleshoe. MU joint with pre-installed NPR plug and pre-installed 1 3/4' ball. MU and ran one 7' tubing joint. MU and ran 7'x 9 5/8' Granite production packer. MU and ran one 7' tubing joint. MU 7' 20 ft PBR assembly with pups. Load tested PBR." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Attempted to MU and run 7' tubing joints. Had to LO out 2 joints." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW due to high winds up to 71 knop. Crane was not able to lift DHPG on to drill floor and could not RU sheave weel for DHPG and chemical injection line in derrick. Meanwhile continued MU and run 3 x 7' tubing joints. Had to LO out 1 joint." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW due to high winds up to 60 knop. Crane was not able to lift DHPG on to drill floor and could not RU sheave weel for DHPG and chemical injection line in derrick." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Installed control line sheave in high strength wire in derrick. Held on to sheave with PRS racking arm to avoid it from moving in the wind." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: POOH to check collar that was changed out on second joint below gauge carrier. Verified correct length on tubing compared to tally." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 110m. The activity was categorized as 'completion -- completion string' and lasted for 7.0 hours. Operational details: Held tool box meeting prior to PU gauge assembly. MU and RIH with DHPG/Asphalthene assembly. Installed one tubing joint above DHPG and positioned assembly in working hight. PU and terminated cable to DHPG. Function checked gauge. Connected chemical injection line. Tested line and installed protector clamps." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 145m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Ran 7' tubing, cable and clamps from 110 m to 145 m MD. Maintained 100 bar pressure on chemical injection line while RIH." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 145m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Installed AFT rollers to HTS and function tested same." "On 2008-01-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 286m. The activity was categorized as 'completion -- completion string' and lasted for 3.2 hours. Operational details: Ran 7' tubing, cable and clamps from 145 m to 286 m MD. Maintained 100 bar pressure on chemical injection line while RIH." "On 2008-01-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 625m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: Ran 7' tubing, cable and clamps from 286 m to 625 m MD. Maintained 100 bar pressure on chemical injection line while RIH. Up weight 90 MT / down weight 85 MT at 500 m MD." "On 2008-01-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 800m. The activity was categorized as 'completion -- completion string' and lasted for 4.5 hours. Operational details: Ran 7' tubing, cable and clamps from 625 m to 800 m MD. Maintained 100 bar pressure on chemical injection line while RIH." "On 2008-01-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 800m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW due to unfavorable wind direction and high winds up to 70 knots." "On 2008-01-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 881m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Ran 7' tubing, cable and clamps from 800 m to 881 m MD. Maintained 100 bar pressure on chemical injection line while RIH." "On 2008-01-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 881m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: WOW due to unfavorable wind direction and high winds up to 70 knots." "On 2008-01-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1322m. The activity was categorized as 'completion -- completion string' and lasted for 8.0 hours. Operational details: Ran 7' tubing, cable and clamps from 881 m to 1322 m MD. Maintained 100 bar pressure on chemical injection line while RIH. LO 1 joint." "On 2008-01-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1620m. The activity was categorized as 'completion -- completion string' and lasted for 6.0 hours. Operational details: Ran 7' tubing, cable and clamps from 1322 m to 1620 m MD. Maintained 100 bar pressure on chemical injection line while RIH. Average running speed is 5,5 joint/hr. Up weight 132 MT / down weight 111 MT at 1500 m MD." "On 2008-01-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1738m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Ran 7' tubing, cable and clamps from 1620 m to 1738 m MD. Pressure dropped from 100 to 25 bar on chemical injection line." "On 2008-01-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1738m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Bled off pressure in chemical injection line and observed for pressure build up. No pressure increase observed. Pressured up to 50 bar and observed that it bled back to 25 bar. Meanwhile serviced PRS and TDS." "On 2008-01-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2428m. The activity was categorized as 'completion -- completion string' and lasted for 13.2 hours. Operational details: Ran 7' tubing, cable and clamps from 1738 m to 2428 m MD. Pressure increased from 25 bar to 35 bar on chemical injection line while RIH. Average running speed was 5,5 joint/hr. Took 4.5 MT weight when entering 9 5/8' tieback hanger at 2412 m MD. PU 8 MT and continued to RIH at slow speed." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2528m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Ran 7' tubing, cable and clamps from 2428 m to 2528 m MD. Pressure increased from 35 bar to 38 bar on chemical injection line while RIH. Average running speed was 5,5 joint/hr. Up weight 195 MT / down weight 130 MT." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2528m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Held tool box meeting with involved personnel. PU and MU DHSV assembly." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2528m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: DHSV got stuck in lower guiding plate on FMS while lowering DHSV assembly through slips. Managed to free slips." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2528m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Removed FMS and lowered DHSV through rotary table. Re-installed FMS. Installed one joint above DHSV. Installed hole cover." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2528m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: RU sheave wheel for single CL to a tugger. Inserted and hoisted in position. PU, flushed and connected CL. Tested CL to 570 bar / 10 min. Bled down pressure to zero and got 210 ml back. Pumped up to 420 bar on control line to maintain DHSV open while RIH." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3023m. The activity was categorized as 'completion -- completion string' and lasted for 13.2 hours. Operational details: Ran 7' tubing, cable and clamps from 2528 m to 3023 m MD. Pressure increased from 38 bar to 45 bar on chemical injection line while RIH. Average running speed was 4 joint/hr due to increased drag. Up weight 227 MT / down weight 137 MT." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3031m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Performed pre-job meeting. MU the last tubing joint and RIH slowly. Stung into top of liner with ratcheting muleshoe approx 4 m before landing out with no-go. Sat down 5 MT and marked pipe 7.69 m off btm of joint #19. Pulled up to up-weight and marked pipe 6.5 m off btm of joint #19. POOH 8 m to confirm tagging depth. Up weight 215 MT / down weight 135 MT. Observed that up-weight was reduced by 12 MT. RIH slowly and verified landing depth." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3031m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Discussed situation with town." "On 2008-01-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: POOH with 3 tubing joints. Took up weight 225 MT / down weight 135 MT. RU to circulate down tubing. Meanwhile re-calculated casing design for production PBR being sheared prior to setting the production packer. Calculated space-out for production PBR." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3006m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Performed line-up check. Attempted to circulate by pumping 100 lpm with cement unit up to 13 bar. No returns observed. Held pressure for 2 min. This confirmed that PBR had not been sheared. RD circulation equipment. PU and MU 6.038 m pup joint according to original space-out." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3007m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: PU and MU tubing hanger with handling tool. Lowered the TH down to rotary. Cut the control lines 3 m above TH and fed the CL through the TH. Plugged off DHPG line. Plugged off spare penetration holes in TH with 1/4' NPT blind plugs. Leak tested all fittings simultaneously through 1/8' test ports to 448 bar /10 min." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3007m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lifted TH to sufficient hight for handling master bushing. Removed FMS and installed master bushing. Installed C-plate and landed TH in same." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3007m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: BO and LD TH landing tool. Wrapped control lines 3 times around hanger neck. Found broken gauge line." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3007m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Dicussed situation with town and decided to re-splice the gauge line." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3007m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: Spliced gauge cable. Fed gauge line through hanger and installed clamp." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3007m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Landed TH in C-plate. BO and LD TH hanger handling tool. Leak tested fitting through 1/8' test port to 448 bar /10 min." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3007m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Attempted to install TH running tool with BX-elevator. Changed to pick-up elevator and re-stabbed TH running tool. MU THRT to communication collar with 8 left hand turns. Connected chemical injection line and TRSCSSV control lines to 1/4' communication ports on top of THRT. Leak tested TRSCSSV line to 570 bar/10 min. Bled off 510 ml. Pressured up and kept 570 bar on TRSCSSV line while RIH. BO THRT piston retaining screws." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: PU TH running string and removed C-plate. Installed bushings. Drained riser down to wellhead using A-annulus overboard line. RIH while taping control lines to landing string and stung into liner PBR. Landed out on the landing shoulder in the tubing head. Stick-up 1.33 m." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested TH in port 1 on surface WH to 70 bar/5 min to verify correct landing. Pressured up function line on THRT to 207 bar to engage TH lock down ring. Pull tested TH to 236 MT to verify hanger lock down." "On 2008-01-29, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pressure tested TH seal through test port 1 on surface WH to 35/450 bar for 5/10 min. Bled down to zero bar when test was verified by StatoilHydro. Meanwhile changed elevator inserts and prepared to PU pumping/testing assembly." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: MU pumping/testing assembly and confirmed line-up with cement unit. Filled tubing with drill water and performed line test to 345 bar/10 min. Meanwhile bled off pressure in chemical injection line and observed for back flow for 30 min." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Opened A-annulus valve. Pressured up tubing against pre-installed NPR plug w/ball to 50 bar/10 min. Volume pumped 186 ltrs. Meanwhile observed no pressure build-up in chemical injection line for 10 min. Pressured up chemical injection line until pressure leveled out at 95 bar." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Closed TRSCSSV and bled off pressure above to 5 bar. Inflow tested TRSCSSV for 10 min. Volume bled off was 30 ltrs. Pumped 44 ltrs, equalized and opened TRSCSSV. Pressured up control line to 570 bar and kept TRSCSSV open." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.8 hours. Operational details: Continued to pressure up tubing to 300 bar. Held pressure for 15 min to set packer and test tubing. PBR sheared at 221.5 bar. Volume pumped was 774 ltrs (Total: 186 + 774 = 960 ltrs). No flow observed from A-annulus. Meanwhile performed a 300 bar/15 min leak-test on chemical injection line." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.8 hours. Operational details: Bled off pressure in tubing to 280 bar. Volume bled back was 50 ltrs. Closed TRSCSSV and bled off pressure above to 210 bar. Volume bled back was 40 ltrs. Inflow tested TRSCSSV to 70 bar/30 min. Bled off pressure above TRSCSSV to 10 bar. Volume bled back was 120 ltrs. Inflow tested TRSCSSV to 270 bar/30 min. Pumped 180 ltrs, equalized and opened TRSCSSV. Bled off pressure in tubing to zero. Volume bled back was 780 ltrs. Kept TRSCSSV open. Closed A-annulus valve. RD pumping/testing assembly. Meanwhile performed SJA with wireline crew." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3028m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Performed pre-job meeting on rig floor. Spotted and RU WL equipment." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 8.5 hours. Operational details: Performed pre-job meeting and reviewed SJA with two different crews (crew change). MU 7' Vam Top x 9' 4 ACME crossover to top of landing string. Installed Seawell pump-in sub. Installed kill hose to pump-in sub. Lined up and pressure tested to 345/10 min against inner Lo-torque valve. Ok. Installed 6 1/2' WL-BOP. Hooked up hydraulic connections to WL-BOP and function tested same. Closed WL-BOP. Performed connection test to 300 bar/5 min against NPR plug in tubing at 3014 m MD. Kept A-annulus vented and observed for fluid returns out A-annulus at surface WH. Volume pumped was 942 ltrs. Bled back 880 ltrs. No returns observed." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 7.5 hours. Operational details: RU WL sheave with 7/32' braided line in TDS and PU to sufficient hight. PU and installed lower WL lubricator section. PU upper WL lubricator section to above connection point. Lowered cable head down to WL-BOP and connected lubricator. Broke connection above WL-BOP and lifted lubricator section 1.5 m. Installed WL toolstring. Attempted to fill up lubricator using cement unit, but ended up using WL test pump. Leak tested rig-up to 25/300 bar for 5 /10 min." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Observed tugger wire and 7/32' braided line was twined together at top of lubricator. Got acceptance from OIM and performed SJA for man-riding operation in derrick with wind speed 36-40 knots to be able to RIH." "On 2008-01-30, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1500m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Equalized and opened blind rams. RIH with WL toolstring to 450 m MDRKB and verified that TRSCSSV was fully open. Continued RIH with WL toolstring from 450 to 1500 m MDRKB." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: RIH with WL toolstring from 1500 to 3000 m MDRKB. Pick up weight 670 kg / slack off weight 760 kg." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3015m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Pressured up tubing to 10 bar with cement unit. Volume pumped was 40 ltrs. RIH and latched plug at 3014.8 m MDRKB. Observed for pressure drop for 15 min when equalizing the plug. No pressure drop observed. Jared plug free and waited for 30 min to let plug elements retract. Confirmed that plug was free. No pressure drop observed." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2972m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: POOH with NPR plug from 3014.8 m to PBR at 2972 m. Made attempt to pass PBR with max overpull of 785 kg. Bled off pressure in tubing to zero and waited another 30 min to ensure that elements was released. Bled back 80 ltrs. No returns on A-annulus. Continued to attempt to pass PBR. Max overpull 900kg. Unable to pass restriction at 2972 m MDRKB, but free to go down." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3020m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Worked to free NPR pulling string from 3020 m to 2972 m. PU weight was 950 kg. Filled tubing up to neddle valve on lubricator and checked for swabbing effect." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3068m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Tensioned up cable to 1700 kg at 2972 m and waited 35 min. Continued to work to free NPR pulling string from 3068 m to 2972 m." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Discussed situation with town and made plans for further operations." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Held pre job meeting with involved personnel. RU hose from cement unit to A-annulus and performed line test 200 bar/5 min. RIH with NPR pulling string to 3000 m. Reduced TRSCSSV CL pressure to 520 bar." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Pressured up A-annulus to 100 bar using cement unit. Volume pumped 786 ltrs. Kept TRSCSSV CL pressure below 570 bar. Worked to free NPR pulling string from 3000 m to 2972.4 m. Observed that restriction had shifted 0.4 m deeper. Not able to pull NPR plug through PBR." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Pressured up A-annulus to 200 bar using cement unit. Volume pumped 710 ltrs. Kept TRSCSSV CL pressure below 570 bar. Worked to free NPR pulling string from 3000 m to 2972.8 m. Observed that restriction had shifted 0.4 m deeper. Not able to pull NPR plug through PBR." "On 2008-01-31, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Closed A-annulus valve. Moved hose from A to B-annulus. Pressured up to 200 bar to equalize pressure against B-annulus. Opened B-annulus valve and bled off pressure to zero. Bled back 1390 ltrs. Closed B-annulus. Menwhile adjusted TRSCSSV CL pressure and RU overboard line to A-annulus." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Lined up cement unit to pump-in sub on rig floor and performed line test to 345 bar. Prepared injection head for 345 bar test. Bled off chemical injection line to zero and inflow tested same. Pressured up the tubing to 35 bar/10 min to test the production packer from below. Volume pumped was 117 ltrs. Kept 570 bar on TRSCSSV CL. Opened A-annulus. No backflow observed. Pressure dropped 0.17 bar. Pressured up the tubing to 345 bar/10 min to test the production packer from below. Volume pumped was 1137 ltrs (total). Kept 570 bar on TRSCSSV CL. No backflow observed. Pressure dropped 1.0 bar. Inflow test of chemical injection line was ok." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3000m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Worked to free NPR pulling string from 3000 m to 2971.0 m. Observed that restriction had shifted 1.0 m higher due to balloning. Not able to pull NPR plug through PBR. Bled pressure back to zero. Volume bled back was 1390 ltrs. Worked to free NPR pulling string from 3000 m to 2972.0 m. Not able to pull NPR plug through PBR." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3089m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with NPR pulling string to 3089 m and tagged TCP gun hanger. Up weight 1060 kg. Put NPR plug on top of TCP gun hanger and jared 10 times without lifting the plug from the hanger. Pulled up 2-3 m to 1200 kg tension and lost 500 kg, before upweight stabilized at 800 kg. Went down and verified tag at 3089 m." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: POOH with NPR pulling tool. Passed PBR and TRSCSSV without any signs of hanging up. Hanged off toolstring in tool catcher." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Observed tugger wire and 7/32' braided line was twined together at top of lubricator. Held tool box meeting. Had to man-ride to sort out wires in derrick. Broke connection above WL-BOP and lifted off lubricator section. LD WL toolstring." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.8 hours. Operational details: Stabbed the WL lubricator. Waited on weather and WL tools to arrive from shore." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.8 hours. Operational details: Untangled the WL wire from the shackle on the tugger line. Cut of 50 m of wire and made new rope socket. Took pull test on the rope socket to 1500 kg. Tested the up stroke on jar, worked at 500 kg." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Held meeting with shore regarding running details." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Re-calibrated the WL BOP." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Made up new WL BHA and installed in lubricator. HW 240 kg." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Leak-tested rig-up to 25bar/5min and 240 bar/10min, against WL-BOP Blind Rams." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3050m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Opened the WL-BOP Blind Rams, and Shear Blind rams. RIH with the NPR plug GS retrieving tool. At 2950 m weight up/down 730/370 kg HW 670 kg. RIH to 3050 m weight up/down 750/370 kg HW 370 kg. Drifted back to 2963m without no obstruction." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3094m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: RIH and latch the NPR at 3094 m (WL depth). Pulled out with the NPR plug, had 200 kg extra pulling weight, Entered the Mule shoe, no obstruction. Kept steady pull of 12 m/min, took overpull of 400 kg at 2975 m, continued pull out of hole. Passed the DHSV with no overpull." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Unable to latch with the tool catcher. HW 390 kg. Held tool talk prior to brake at the WL BOP." "On 2008-02-01, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Applied 150 bars to the grease injection head. Pressure up the well to 80 bars, 340 litres, closed the DHSV and bled of the pressure to 10 bars above the DHSV and inflow tested same for 10 min." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Applied 80 bars to the well and opened the DHSV. Bled of the pressure of the well, same volume in return 340 litre." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Broke the lubricator and laid out the BHA with NPR plug, no damage to the NPR plug." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.8 hours. Operational details: R/D the WL lubricator, the GIH, the WL BOP and disconnected the BCU." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Held tool box talk prior to retrieve the TBG landing string. R/D the control lines." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Rigged down control line sheave." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Held tool box talk prior to L/O the 7' landing string. Attempted same." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Problems with elevators malfunction, investigated same. Changed out elevators and function tested same." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Held tool box talk prior to use tuggers to retrieve the 7' landing string. Picked up and laid out 7' landing sting." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Cleared rig floor, casing tong, Baker control line drum, Gauge/inj. Line drum and PS-30 slips." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Held tool box talk prior to installation of the BPV. Picked up the PBV and ran in same on tugger and installed same." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Held tool box talk prior to nipple down the stack. Nippled down BOP and set back into cradle, laid out riser." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed dart in BPV." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered down tension cylinder to centralizer deck." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk prior to lower down the Co-flex hose onto the XMT deck." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Lowered the Co-flex hose onto the XMT deck." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to terminate the control lines." "On 2008-02-02, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed the communication collar." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Terminated the control line in the well head." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed the spacer spool. Found the protection cover for hydraulic outlets at the master bushing laying on the well cover on XMT deck." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held time out regarding dropped object from drill floor to the well head: 20m, 5 kg." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk prior to install the master bushing and installed same." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed master bushing." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 9.0 hours. Operational details: Installed extension spool and torqued up same. Pressure tested void to 30/345 bars 5/10 min. Pressure tested VG 63 seal 35 bars 10 min. Installed gauge outlet. Meanwhile had time out with dayshift regarding dropped object." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box talk prior to R/D scaffolding and removal of hatch cover. Performed same." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up and installation of the X-mas tree." "On 2008-02-03, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.2 hours. Operational details: Picked up, landed, orientated and installed the X-mas tree. Installed WV spool outlet and production co-flex hose." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: Made up 2' 1502 hose to the KWV outlet. Torqued up the PWV spool outlet and the production co-flex hose." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pressure test the production line and the X-mas tree." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lined up and flushed the lines to the X-mas tree" "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Completed flushing of lines to the X-mas tree." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Leak tested X-mas tree connections to 30/345 bars 5/10 min." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk prior to flush X-mas tree and production flow line prior to leak test of same." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Awaited confirmation of correct torqued up flow line." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Checked remote panel to operate X-mas tree valves. Found too low fluid level." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Flushed production flow line into the separator." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Lined up and leak tested production flow line 50/180 bars 5/10 min." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to inflow test LMV and HMV against BPV." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Pressured up to 240 bars against BPV. Inflow tested LMV and HMV, 230 bars diff." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to retrieve the dart and the BPV." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Removed tree cap, had to pump out same. Retrieved the dart and the BPV. Re-installed the tree cap." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Leak tested tree cap to 30/345 bars 5/10 min." "On 2008-02-04, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Pressure tested BOT control line exit blocks for DHSV to 570bars/15 min. Measured return fluids from control line 225 ml. Removed the Co-flex support frame at the X-mas tree, and transferred to the welders shop for modification. Continued operation on F-4" "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Held prejob meeting with all involved, including Maersk Production." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Installed lo-torq valve on kill valve on XMT. Hooked up 2' HP-hose from lo-torq valve to cement pump kill line valve in moon pool." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Flushed line from cement unit to XMT, observing for returns in needle valve on XMT cap." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Closed KV. Leak tested line from cement pump to KV to 250 bar/10 min. No leak observed through needle valve on XMT cap. Bled pressure down to 20 bar, to cement pump. Closed SV and needle valve on XMT cap. DHPG pressure = 277,1 bar." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Opened MMV. Opened HMV. Pressured up well to 30 bar with cement pump. Confirmed pressure increase on DHPG. Opened DHSV w/460 bar control line pressure." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Continued to pressure up well to 240 bar (750 liter) with cement pump. Pressured up chemical injection line to 230 bar with Well Dynamics test pump. Leak tested termination block for chemcial injection line on wellhead to 230 bar/10 min." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Closed MMV. Bled off pressure above MMV to 10 bar. Inflow tested MMV to 230 bar/10 min. Equalized MMV with 240 bar. Opened MMV. Closed HMV. Bled off pressure above HMV to 10 bar. Inflow tested HMV to 230 bar/10 min. Equalized HMV with 240 bar. Opened HMV. Bled ppressure in well to 0 bar to cement pump. Bled back 710 liter. Counted 3 cycles on ProFire firing head on TCP guns." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Schlumberger TCP performed training pulses with cement pump. Schlumberger sent firing command ,with cement unit, to E-Fire firing head in TCP guns. Bled down well pressure to 0 bar to cement unit. Closed TKV and Lo-torq valve. The TCP guns fired after waiting the programmed time delay of 10 minutes. Wellhead pressure / DHPG pressure increased to 31/ 308 bar. Closed DHSV. Bled down pressure above DHSV to 0 bar to the flowline. Monitored WHP in XMT for 30 minutes to verify DHSV integrity. No pressure buildup observed." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Closed valve to cement pump kill line in moon pool to isolate 2' HP-hose to KV on XMT." "On 2008-02-11, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Performed well hand over activiities. Verified that all valves on XMT and DHSV were closed. Handed well over to Maersk production at 17:00. ****************END OF OPERATIONS****************" "On 2009-03-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 3.5 hours. Operational details: Waited on Mærsk Production to hand over well to Volve D&W. Meanwhile performed 5-yearly maintenace on choke manifold." "On 2009-03-13, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 5.5 hours. Operational details: Waited on Mærsk Production to shut in well and inflow test HMV to 120-5 bar/10 min and DHSV to 120-5 bar/30 min. Had 2.3 bar drop/10 min on HMV and 0.2 bar drop/30 min on DHSV. Meanwhile performed 5-yearly maintenace on choke manifold and loosened bolts on kill ving valve on BOP in preparation for 5-yearly maintenance." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Bled off pressure to 0 bar above DHSV. Confirmed valve status and handed over well to drilling at 01:00." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Transferred HMV and DHSV to local controled panel (wireline lock-out mode). Connected Seawell pump and tested line up." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Installed test and bleed manifold from moonpool outlet to XMT KWV. Prepared bleed down hose and valves from KWV to closed drain." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Flushed lines and attempted to perform line test to 30/200 bar for 5/10 min from cmt unit to KWV through test and bleed manifold. Had 8 bar increase on low pressure test. Investigated situation. Performed 'line test' for cmt unit seperatly. Ok. Performed line test to 30/200 bar for 5/10 min from cmt unit to KWV through test and bleed manifold." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Opened KWV and attempted test XMT cross. Pressure dropped from 20 to 8 bar while pumping and from 26 bar to 11 bar on second attempt. Checked line-up for leaks. No leaks observed. Opened SV. Flushed through XMT through tree cap needle valve. Closed SV and re-attempted to test XMT cross. Pressure dropped from 30 to 8 bar. Closed LTV1 and performed a second line test to 30 bar/5 min. Ok. Opened LTV1 and re-attempted to test XMT cross without sucess." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Closed MMV to establish if it was HMV or PWV that was leaking. Re-attempted to test XMT cross without sucess." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Operated and greased up PWV." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Verified PWV, SV and HMV were closed. Leak tested XMT cross to 30/200 bar for 5/10 min using cmt unit and 100% MEG. Had 2.4 bar drop (1.2%)/10 min. Bled off pressure to 0 bar to platform closed drain. Verified no pressure below treee cap and removed same." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held tool box talk for installing WL riser and lubricator and change elevator. Lifted WL riser sections and BOP with Top Drive using double lift arrangement. Lowered and stabbed on to XMT connection." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Changed elevators and PU lubricator. Meanwhile pressure tested shear ram on WL BOP to 30/200 bar for 5/10 min. Ok." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Man-rode to turn WL sheave wheel." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: MU combination toolstring in riser and stabbed on lubricator with in-situ sub." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Verified that toolstring was sitting in toolcatcher. Opened SV 10 turns and opened KWV. Filled riser with 100% MEG from cmt unit. Leak tested WL riser, BOP and lubricator to 30/200 bar for 5/10 min using cmt unit and 100% MEG. Ok. Bled off pressure to 0 bar. Closed SV and KWV." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Performed well control exercise with Seawell, Schlumberger and Mærsk crew." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Opened HMV, KWV and SV 10 turns. Filled well above DHSV with 7.7 m3 100% MEG. Equalized and opened DHSV at 93 bar. Closed KWV and bled off pressureto 0 bar in manifold." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 485m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Opened SV with 45 turns. RIH with combination toolstring on 7/16' EWLL to 485 m and took pick up weight." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 498m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Attempted to RIH through DHSV, but found solid hold up depth at 498 m." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 485m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Changed out MEG tanks and re-filled MEG on cmt unit. Meanwhile held tool box talk prior to equalizing and opening DHSV. Performed well control exercise with Seawell, Schlumberger and Mærsk crew." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 485m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Opened LTV1 and LTV2. Equalized pressure to 90 bar and opened KWV. Pumped 8.95 m3 100% MEG into well and observed pressure drop from 90 to 69 bar. This confirmed that DHSV was open/partly open." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 485m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Attempted to RIH through DHSV, but found solid hold up depth at 498 m. Discussed further options." "On 2009-03-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 485m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Functioned DHSV closed/open twice to remove possible debris. Had 3.0 dl return when closing DHSV and pumped 4.25 dl when opening DHSV. Had good indication of DHSV being in open position." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 498m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Attempted to RIH through DHSV and experienced a 1 m drop of the toolstring after initial hold up. Made several more attempts to run through DHSV." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3260m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: RIH with toolstring through DHSV to 515 m and pulled back up to ensure valve was fully open. Continued RIH with combination toolstring on 7/16' EWL from 485 m to 3027 m (tally dyp). Hung up at 7' liner PBR and made several attempts to enter 7' liner. Continued RIH with combination toolstring from 3027 m to 3260.5 m (log dyp). RIH tension was 1900 lbs and PU tension was 5100 lbs at 3250 m MD. RIH speed was 30 m/min. RIH speed inside 7' liner was 20 m/min. Tension inside 7' liner was higher than simulated (60% of max safe pull to be able to break weakpoint)." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3260m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Tagged top of TCP guns at 3260.5 m (ref open hole log)/ at 3258.5 m (ref pip-tag in tally). Made GR-CCL correlation log from 3260.6 m to 3029 m (top of 7' liner)." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH with combination toolstring on 7/16' EWL from 3029 m to OOH. Ran carefully through DHSV at 497 m MD. Pulled cable head into tool catcher." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Closed SV partly and verified toolstring out of hole. Recorded SIWHP 81 bar. Closed HMV and bled down pressure above to 5 bar." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Inflow tested HMV 81 -5 bar/10 min ok. Opened KWV and SV 10 turns. Bled off pressure to zero to closed drain and purged riser with Nitrogen. Closed KWV. Bled off remaining pressure in lubricator through needle valve. Closed SV." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Broke lubricator at in-situ sub and LD combination toolstring. Found centered circular impression on lead impression block confirms that part of running tool for TCP gun hanger was lost in hole and is sitting at the top of the TCP gun hanger." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Installed PLT toostring in riser and MU in-situ sub. Leak tested in-situ sub to 30/200 bar for 5/10 min. Ok." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Opened KWV. Equalized and opened HMV using cmt pump and 100% MEG. WHP was 85 bar. Closed KWV." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3030m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: RIH with PLT toolstring on 7/16' EWL from surface to 2929 m MD. Ran carefully through DHSV at 492 m. Performed station log and checked readings against DHPG. Continued RIH with PLT toolstring on 7/16' EWL from 2929 m to 3030 m MD." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Logged PLT down/up and performed shut-in calibration passes from 3030 m to 3255 m MD. Pass 1: Down/up speed: 10 m/min Pass 2: Down/up speed: 20 m/min Pass 3: Down/up speed: 30 m/min Pass 4: Down/up speed: 40 m/min" "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: RIH with PLT on 7/16' EWL from 3030 m to 3255 m MD. Took stationary PLT readings at : 3245 m MD 3233 m MD 3200 m MD 3154 m MD POOH with PLT toolstring from 3154 m to 3080 m MD. Spinner response appr 2.0 RPS. Moved even further up to 2915 m. Still spinner response 2.0 RPS. Decided to go down to 3080 m again." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 7.0 hours. Operational details: Beaned up well in increments to 4500 Sm3/d. Obtained stable FBHP ( less than 0.1 bar variance for 1 hr) of 276,6 bar at DHPG." "On 2009-03-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Logged PLT down/up and performed high rate passes from 3030 m to 3255 m MD. Pass 1: Down/up speed: 10 m/min" "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Logged PLT down/up and performed high rate passes from 3030 m to 3255 m MD. Pass 2: Down/up speed: 20 m/min Pass 3: Down/up speed: 30 m/min Pass 4: Down/up speed: 40 m/min" "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH with PLT on 7/16' EWL from 3030 m to 3255 m MD. Took stationary PLT readings at : 3245 m MD 3233 m MD 3200 m MD 3154 m MD POOH with PLT toolstring from 3154 m to 3080 m MD." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Choked back on well in increments to 3000 Sm3/d. Obtained stable FBHP ( less than 0.1 bar variance for 1 hr) of 283,7 bar at DHPG." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Logged PLT down/up and performed medium rate passes from 3030 m to 3255 m MD. Pass 1: Down/up speed: 10 m/min Pass 2: Down/up speed: 20 m/min Pass 3: Down/up speed: 30 m/min Pass 4: Down/up speed: 40 m/min" "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with PLT on 7/16' EWL from 3030 m to 3255 m MD. Took stationary PLT readings at : 3245 m MD 3233 m MD 3200 m MD 3154 m MD POOH with PLT toolstring from 3154 m to 3080 m MD." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 3.8 hours. Operational details: Choked back on well in increments to 1500 Sm3/d. Obtained stable FBHP ( less than 0.1 bar variance for 1 hr) of 290,2 bar at DHPG." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3255m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Logged PLT down/up and performed medium rate passes from 3030 m to 3255 m MD. Pass 1: Down/up speed: 10 m/min Pass 2: Down/up speed: 20 m/min Pass 3: Down/up speed: 30 m/min Pass 4: Down/up speed: 40 m/min" "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2929m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: POOH with PLT toolstring on 7/16' EWL from surface to 2929 m MD. Performed station log and checked readings against DHPG. Read 290.1 bar." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2929m. The activity was categorized as 'workover -- wait' and lasted for 1.0 hours. Operational details: Shut in well. Recorded SIWHP was 117 bar." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: POOH with PLT toolstring on 7/16' EWL from 2929 m to surface. Ran carefully through DHSV at 492 m. Pulled cable head into tool catcher. Closed SV using 45 turns to verify BHA OOH. Closed HMV." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Opened SV 10 turns. Opened KWV and bled off pressure in XMT, riser and lubricator to 5 bar to closed drain. Closed KWV and SV." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Inflow tested HMV 117 -5 bar/10 min. Had 1.14 bar (1%) drop/10 min. Opened KWV. Equalized and opened HMV using cmt pump and 100% MEG." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Closed DHSV using Seawell pump on drill floor. Bled off pressure to 113 bar above DHSV. Opened KWV. Bullheaded 3 m3 100% MEG into well using cmt pump." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Bled off pressure above closed DHSV from 113 bar to 63 bar." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Closed KWV. Closed MMV. Opened PWV and bled down XMT and flowline to 5 bar. Closed PWV. Inflow tested MMV to 63 -5 bar/10 min. Had 0.11 bar (0.2%) drop/10 min." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Opened KWV and PWV. Equalized and opened MMV using cmt unit and 100% MEG." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Bled off pressure in XMT/above DHSV through PWV and flowline to 5 bar. Closed PWV and KWV." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Inflow tested DHSV to 117 -5bar/30 min. Had 1.32 bar (1.1%) increase/30 min. Meanwhile had tool box talk prior to breaking down lubricator and toolstring." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Opened KWV. Bled off remaining 5 bar above DHSV to closed drain." "On 2009-03-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Opened SV. Bled off pressure/drained XMT, riser and lubricator to closed drain." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Continued bleeding off pressure/drained XMT, riser and lubricator to closed drain." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Purged XMT, riser and lubricator with nitrogen 3 times due to grease in lubricator. Closed KWV and SV." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Broke lubricator at in-situ sub. Lifted out and LD PLT toolstring. No marks or damage observed on tool. No obvious explanation why in-line spinner did not work. Cut cable." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: LD lubricator and RD sheave wheels. Split lubricator at drill floor, preserved and moved to cantiliver. Cleared rig floor of WL equipment." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Installed 10 mT lift cap on WL riser and installed manual elevator on riser section as part of double lift arrangement from TDS. Detached riser from BOP's and LO same." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.5 hours. Operational details: Lifted WL BOP's using double lift arrangement from TDS and transferred to moonpool overhead crane." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Disconnected and lifted out lower WL riser section and XO from XMT using double lift arrangement from TDS. Installed hatch on weather deck." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Installed XMT tree cap. Hooked up hose from Seawell test pump on drill floor to test cap on XMT." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Leak tested SV to 30/345 bar for 5/10 min. Good test. Bled off pressure to closed drain." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: RD cmt test line and bleed off manifold from KWV." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Leak tested tree cap and XMT cross to 30/345 bar for 5/10 min using Seawell test pump and 100% MEG. Good test. Bled off pressure. Installed cap on KWV and removed 1/2' plug. Leak tested KWV to 30/345 bar for 5/10 min using Seawell test pump and 100% MEG. Good test. Bled off pressure. Installed 1/2' plug in KWV cap. Leak tested KWV cap to 30/345 bar for 5/10 min using Seawell test pump and 100% MEG. Good test. Bled off pressure. Disconnected Seawell test pump from XMT tree cap and closed needle valve. Disconnected local control panel for HMV and DHSV and re-established platform permanent control system." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Handed well over from Volve D&W to Mærsk Production." "On 2009-03-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Cleared rig floor off remaining WL equipment. Cleaned rigfloor with dedicated grease wash." "On 2010-09-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Skidded rig to F-12." "On 2010-09-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Changed to workover hatch on F-12." "On 2010-09-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 4.5 hours. Operational details: Waited for Production Department to bean up F-14 and shut in F-12 for leak testing and handover. Meanwhile built new cable head (4/3-2005 lbs) and leak tested cable rams in BOP." "On 2010-09-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 5.0 hours. Operational details: Waited on production department to prepere well for handover. Meanwhile held prejob meeting with all night shift personnel involved in operation." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Took over well. Checked valve status." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 1.0 hours. Operational details: Prod. department installed isolation certificate on remotly operated valves on well." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Leak tested x-mas tree cross. 20/170 bar for 5/10 min." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Removed KWV cap and rigged up chiksan valves. Leak tested bleed off hose against closed KWV. 20/180 bar for 5/10 min." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Removed tree cap and installed lower riser and BOP. Leak tested riser connections and BOP shear seal. 20/180 bar for 5/10 min. Installed upper riser. Prepared lubricator for lifting." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: RU lubricator and GIH in elevator. Installed BHA #1 and stabbed on. Filled rig-up with MEG using platform MEG injection system. Checked toolstring." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Held pre-job meeting with involved personnel." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Leak tested rig-up to 20/170 bar for 5/10 min. Opened HMV and equalized TRSCSSV with MEG using platform MEG injection system. SIWHP 82 bar. Equalized and opened SV." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1000m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: RIH with BHA #1, PLT logging string, to 1000 m MDRKB." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1000m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Performed spinner calibration passes at 10/20/30/40 m/min up/down." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3130m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Continued RIH to 3130 m." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2929m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Performed depth correlation with GR/CCL. Radioactive marker at 3091.7 m. Pulled up to 2929 m (DHG) and took stationary reading. Temp. = 105 C deg. Press. = 311,98 bar." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Ran PLT shut in passes from 3250 to 3080 m at speed 10/ 20/ 30/ 40 m/min. Up / Down. Took stationary readings at 3080, 3250, 3200 and 3155 m. Pulled up and placed PLT at 3080 m." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Beaned up well to approx. 5000 Sm3/d against test separator." "On 2010-09-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Waited for stable flow." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Continued waiting for stable flow. Stabilized flow rate at approx. 5050 Sm³/d." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Took stationary reading for 5 min at depth 3080 m. Attempted to RIH at various speeds. Max speed was 80 m/min. Stopped at various depths between 2985 and 3015 m." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Reduced flow rate to 3000 Sm³/d." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Waited for stable flow rate." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Took stationary readings at 3080, 3155, 3200 and 3250 m." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Logged flowing passes between 3030 and 3250 m. Logged down at 40 m/min and up at 10/20/30/40 m/min. Unable to log down passes at 10/20/30 m/min. Positioned toolstring at 3080 m." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: Reduced flow rate to 1500 Sm3/d and stabilized." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3080m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Logged flowing passes between 3000 and 3250 m. Logged down at 40 m/min and up at 10/20/30/40 m/min. Unable to log down passes at 10/20/30 m/min. Positioned toostring at 3000 m. Shut in well." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Closed well. WHP = 89 bar. Bled down and inflow tested HMV. Bled down and flushed lubricator with N2. LD and inspected BHA #1." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Prepared and checked BHA #2, CCL, DPU and 5,72' EVO bridge plug. Lifted toolstring to rig floor." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Held tool box meeting on rig floor. Installed BHA #2 into lubricator. Added 25 ltr Ramex into riser. Leak tested QTS to 20/170 bar for 5/10 min. Equalized with N2 across HMV and opened well. WHP 98.6 bar." "On 2010-09-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 800m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH with BHA #2, EVO bridge plug to 800 m." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3220m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Continued RIH with 5,72' EVO plug to 3220 m." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3210m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Performed depth correlation passes. POOH to setting depth and activated DPU. Installed plug with mid element at 3210 m and top plug at 3209,3 m. Lost 400 lbs. WHP 98,7 bar." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: POOH with BHA #2." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Closed well. WHP = 98.6 bar. Bled down and inflow tested HMV." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Bled off and flushed lubricator with N2." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: LD toolstring. Running tool OK." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Opened HMV and bled down pressure above DHSV against test separator to 1 bar. Pumped 200 litres of MEG into well. Inflow tested DHSV." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Leak tested x-mas tree cross. 20/100 bar for 5/10 min." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Held prejob meeting regarding RD WL equipment with all personnel involved in operation. LD lubricator onto catwalk machine. (HTS)" "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Disconnected and lifted upper riser to rigfloor with top drive. Disconnected and lifted BOP away in moon pool area. Disconnect and lifted lower riser to rig floor." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Installed x-mas tree top cap and KWV cap. Leak tested both. 20/345 bar for 5/10 min." "On 2010-09-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Cleaned up in wellhead area. Transfered controll of DHSV and HMV to platform system. Handed well over to Maersk Prod. department. Meanwhile started to skid rig to next location. --------------------------------- END OF OPERATION---------------------------------------------" "On 2014-11-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Stril Luna arrived Maersk Inspirer. Spotted some equipment. Wind picked up above 40 knots, had to wait for further spotting." "On 2014-11-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.8 hours. Operational details: Waited on weather prior to lift and spot containers from vessel." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: Waited on weather prior to spotting equipment." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held toolbox talk with all involved prior to spotting equipment. Meanwhile boat positioned longside rig." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.5 hours. Operational details: Spotted Altus and Halliburton equipment on pipedeck." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.0 hours. Operational details: Checked alignment on WL winch and fine tuned add on. Secured same to pipe deck. Pulled cables between the different containers." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.5 hours. Operational details: Spotted wellhead pump and filled with correct fluid. Connected add on drum together with winch. Maersk electrician checked WL equipment due to punch list from onshore." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Maersk performed a thorough check of the Altus equipment due to the findings onshore. Meanwhile unpacked equipment from conatiners and prepared for BOP test." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Continued to prepare equipment and hoses for testing of BOP. Meanwhile continued to check equipment together with rig electrician." "On 2014-11-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.5 hours. Operational details: Performed low pressure test of BOP. Meanwhile continued to check equipment together with rig electrician." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Continued with high pressure test on BOP. Meanwhile continued to check equipment together with rig electrician." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Function tested WL unit & winch. Hooked up logging container to power. Meanwhile performed area inspection on wellhead and discussed procedure for R/U WL riser on XMT." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Spotted parts for grease injection head and toolcatcher. Spotted riser parts for building same on drill floor." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Performed toolbox talk prior to start building riser and lubricator pieces." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Built the riser and lubricator sections horizontally on the pipe handling system. Meanwhile notified production dept to start shut in well F-12." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.0 hours. Operational details: Hooked up remaining containers to fire and gas and completed check of Altus winch and logging unit. Meanwhile prepared correct fittings to be hooked up to HMV to DHSV on wellhead." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Rigged up sheave wheel and prepared spreader beam for lubricator." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Waited on production to obtain good test on XMT valves. Not able to obtain good test. Had to grease HMV and MMV. Meanwhile preapred cablehead and tested Halliburton toolstring." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Handed well over from Production department to Drilling and well." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed toolbox talk on drill floor prior start R/U on well. Work permit for start rigging on XMT not activated or prepared." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: Had to wait for WP to be approved for rigging of WL equipment. Meanwhile prepared manifold and chicksan on wellhead." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Held SJA for rigging of WL equipment on XMT." "On 2014-11-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Rigged up chicsan and low torque on KWV." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Continued to rig up on wellhead. Completed rigging up manifold on KWV. Observed 35 bar pressure in XMT cross." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Checked valves and inlets into XMT cross for possible leaks, together with production operator. Found that valve for MEG pump was leaking into XMT cross. Closed another valve on the MEG inlet line. Bled off pressure." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Installed wireline hatch and disconnected top cap on XMT." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Lowered bottom riser and X-over. Installed BOP and hooked up lines. Function tested BOP. Filled lower riser and BOP with MEG using MEG pump and closed upper ram for testing lower riser." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Rigged riser from BOP up to drill floor." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Rigged up lubricator and hoses on drill floor. Attached sheave wheel in spreader bar in top drive. Lifted up lubraicator. Meanwhile prepared Halliburton toolstring on drill floor." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to picking up BHA." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.5 hours. Operational details: Installed BHA#1 7' EV0 plug into lubricator. Stabbed lubricator and tested communication with toolstring." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Held toolbox talk prior to leak test the R/U." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.9 hours. Operational details: Erected barriers for leak testing and got production department to fill riser with MEG using MEG pump. Leak tested R/U to 20/345 bar using Altus pump. Observed leak in the test hose from the pump during low pressure test." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed hose and continued with leak test." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.8 hours. Operational details: Leak tested R/U and kill wing chicksan manifold to 20/345 bar for 5/10 minutes using 100% MEG. Equalized DHSV using MEG from production system. DHSV equalized and opened at 51 bar. Equalized and opened SV." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1000m. The activity was categorized as 'workover -- other' and lasted for 2.2 hours. Operational details: RIH w/BHA #1 (7' EV0 plug) from surface to 1000 m. WHP 51 bar. Observed loss in communication with toolstring. Signal came back again. Continued to RIH. Pick up weights approx. 700 lbs higher than simulated values." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1400m. The activity was categorized as 'workover -- other' and lasted for 0.3 hours. Operational details: Continued to RIH from 1000 m to 1400 m. Lost commuincation with toolstring. Trouble shooted equipment. Observed communication on and off. Checked surface equipment and trollex. Observed cmmunication falling out when running in hole, but no clear pattern. Decision made to POOH." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: POOH w/BHA #1 from 1400 m to surface. WHP 50 bar." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Closed SV & HMV and inflow tested same. Purged riser with N2 prior to break lubricator." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held Toolbox talk prior to lift L/D BHA#1" "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.3 hours. Operational details: Broke lubricator and L/D BHA#1." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Halliburton checked toolstring components and cablehead. Not able to detect any defects. Decision made to change cablehead and run complete back up string." "On 2014-11-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Re-buildt cable head. Meanwhile Altus checked tension head on WL winch: Winch weight Calibration weight 1000 lbs 950 lbs 2000 lbs 1800 lbs 3000 lbs 2680 lbs 4000 lbs 3500 lbs The calibrated Halliburton weight will show correct tension" "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Continued to re-build cable head. Time consuming to build due to stiff cords on 7/16' cable together with narrow holes in cablehead cone." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.6 hours. Operational details: Lifted tools to rig floor for testing of toolstring through cablehead. Meanwhile held toolbox talk for installing the BHA into lubricator." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Installed toollstring into lubricator and Leak tested QTS to 20/345 bar for 5/10 min. Meanwhile held toolbox talk for the plug run." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Opened HMV and equalized acoss swab using well pressure." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- other' and lasted for 1.7 hours. Operational details: RIH w/BHA #2 7' EVO plug from surface to 1400 m. WHP 51 bar. Performed well control drill: Leakage in grease injection head. Stopped each 300 meters to perform P/U weight." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3135m. The activity was categorized as 'workover -- other' and lasted for 2.1 hours. Operational details: Continued to RIH from 1400 meter to 3135 m. Stopped each 300 meters to perform P/U weight." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3150m. The activity was categorized as 'workover -- other' and lasted for 0.9 hours. Operational details: Correlated BHA across interval 3135 - 3050 m . Set plug with mid packer element at 3150 m. Observed 400 lbs drop in tension. WHP 47 bar." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.1 hours. Operational details: POOH with BHA#2 from 3150 m to surface. Hung slightly up in the packer area. Continued to POOH." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Closed SV. Had to wait on production department for bleeding of, due to problems with a gas compressor." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 1.2 hours. Operational details: Bled of lubricator and inflow tested SV & HMV. Purged lubricator with N2." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to L/D toolstring." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Broke lubricator and L/D BHA #2." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Lifted Halliburton perforating toolstring to drill floor and started to prepare guns." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Held toolbox talk prior to arm the perforating guns." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.6 hours. Operational details: Installed BHA #3 (4 5/8' Perforating gun) into lubricator. Stabbed lubricator and tested QTS to 20/345 bar for 5/10 min. Equalized and opened SV and HMV. WHP 46 bar." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3135m. The activity was categorized as 'workover -- perforate' and lasted for 3.6 hours. Operational details: RIH w/BHA #3 (4 5/8' Perforating gun) from surface to 3135 meters. WHP 46 bar. Stopped each 500 meters and pulled up 50 meters. Depth P/U weight 500 m 1410 lbs 1000 m 2130 lbs 1500 m 2950 lbs 2000 m 3650 lbs 2500 m 4400 lbs 3000 m 4900 lbs" "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3135m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Performed three correlation passes across interval 3135 - 3050 m. Positioned gun with top shot at 3126,2 m & bottom shot at 3130,7 mMD. WHP 45 bar." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 3131m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Activated perforation guns. Observed current increase and drop in tension of 200 lbs. No change in WHP at 45 bar. Started POOH." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 480m. The activity was categorized as 'workover -- perforate' and lasted for 2.1 hours. Operational details: POOH with BHA #3 from 3131 m to 480 m. WHP 45 bar." "On 2014-11-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 480m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to take guns out of hole. Included toolbox talk for rigging down WL equipment." "On 2014-11-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Continued to POOH from 480 m to surface." "On 2014-11-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.5 hours. Operational details: Closed SV & HMV and inflow tested for well handover. Purged riser with nitrogen." "On 2014-11-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: Broke lubricator and L/D BHA#3." "On 2014-11-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.3 hours. Operational details: Closed upper BOP ram. Opened HMV and closed DHSV for inflow test of same. Had 40 bar delta P. Test OK - 0 bar/30 min. Bled down pressure above DHSV to 0 and closed HMV." "On 2014-11-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Rigged down lubricator. Rigged down riser above BOP. Disconnected BOP and rigged down same. Disconnected lower riser from XMT." "On 2014-11-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.3 hours. Operational details: Mounted top cap on XMT. Disconnected chickasn on kill wing cap and mounted kill wing cap. Pressure tested Top cap & KW cap to 20/345 bar for 5/10 min. Change WL hatch with permanent hatch. Prepared for skidding to F-1C. ----------------------------------------- END OF OPERATION ------------------------------------------------" "On 2016-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Prepared to skid cantilever" "On 2016-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting to skid cantilever" "On 2016-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Removed stairs and bridge to cantilever" "On 2016-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.8 hours. Operational details: Skidded cantilever to F-12 slot, 0.5m to port , 4.56m forward and 0.5m to starboard" "On 2016-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Removed moon pool hatch on F-12 and confirmed cantilever position. Installed split hatches on F-12" "On 2016-08-14, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for rigging up wire line equipment in moon pool and drill floor" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Removed well cap on F-12. Installed lower riser joint and WL BOP" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Connect WL control lines and hoses to BOP. Function tested BOP Rigged up kill hose to tree P/U upper WL riser joint Lifted WL equipment to rig floor" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting w/ new crew" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed upper riser joint on top of BOP Meanwhile continued to open rig BOP for inspection" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed BX inserts to 3.5in Meanwhile continued to open rig BOP for inspection" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Continued to R/U WL equipment above RKB Meanwhile continued to inspect and clean rig BOP. M/U WL lubricator on HTS and installed hoses on same. Filled A and B annulus." "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lifted lubricator from HTS to TDS" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Built cable head and tested same Meanwhile worked on flow line and cleaned BOP from cement" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U tool string w/ deep set plug BHA (run#4)" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: M/U tool string, installed kill hose onto the tree" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to fill and pressure test WL rig up" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Flushed lines w/ 50/50 MEG. Filled WL riser and lubricator" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pressure tested WL rig up to 20/345bar for 5/10min" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to bullhead the well" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Opened MV and HMV. Observed pressure inside tree increased to 55 Bar. Applied 520 bar on control lines for DHSV. Performed line test and open KWV. Pumped 3 m3 50/50 MEG/SW with cement unit @ 1100l/min - 83bar" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped 10m3 Wash pill at 1300l/min - 91bar" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Bullheaded well with sea water at 1300l/min, +/- 90 Bar. After pumped 40m3, standpipe pressure started to increase slowly. Final circulation pressure 151bar" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped 10m3 MEG/SW with cement unit at 1100l/min SIWHP when stopped pumping 55bar" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.5 hours. Operational details: Equalized and opened SV. RIH with WL to 3010m." "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.8 hours. Operational details: Correlated depth w/ BHA (run#4). Correlation interval 2850m-3005m" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Trouble shoot winch after not able to achieve stable running speed with winch. Suspected overheating of hydraulic system" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Set plug w/ mid packer element at 3003 m. Confirmed plug set w/ tagging" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.2 hours. Operational details: POOH from 3003 m to surface. Average pulling speed 22m/min Meanwhile performed TBT for pressure testing of plug" "On 2016-08-15, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Closed SV and inflow tested same Meanwhile lined up cement unit for pressure test plug" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Pressure tested deep set plug to 20/260bar for 5/10 minutes. Good test" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.8 hours. Operational details: Bled off pressure above deep set plug to close drain to 10bar. Performed inflow test of deep set plug. Good test" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Bled down pressure from tubing. Closed HMV, confirmed SV and KWV closed L/D BHA" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: M/U shallow set plug BHA (run #5), installed same into lubricator. Leak tested lubricator/QTS to 20/345bar 5/10min. Opened HMV, SV" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: RIH shallow set plug to 256m" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Correlated BHA across interval 200 - 300m . Set plug with mid packer element at 249m. Tagged plug. POOH w/ setting tool to lubricator" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Lined up cement pump and pressure tested shallow set plug to 20/230bar for 5/10min. Good test" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Closed HMV,KWV and SV, verified no pressure in XT" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Started R/D wireline equipment" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting w/ oncoming crew to R/D WL equipment" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: L/D plug setting tool" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: R/D lubricator, moved same from the rig floor" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D upper wire line riser joint" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Disconnected control lines and hoses to WL BOP and pulled same to rig floor Meanwhile prepared to pull Fox hole" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/D WL BOP and lower riser joint. Lifted BOP to pipe deck" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for rearranging well hatches in moon pool" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Removed hatches on F-12 and F-7 and beam between slots" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed master bushing, installed chains to TDS and attached to XMT as per lifting plan, with double securing" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued w/ attaching lifting arrangement to XMT Meanwhile performed BOP test No.2 (low pressure only) to 20bar" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed high pressure test on BOP. Test No.2 to 345bar" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued to rig up to pull XMT. Took 1t tension with TDS and disconnected Greyloc clamp below XMT Meanwhile performed BOP test No 1 to 20/345bar for 5/10 min" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lifted XMT to Moon pool and transported to skid according to lifting plan. Meanwhile lined up for BOP pressure test No. 3" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Continued to move/handle XMT to moon pool hatch Meanwhile performed BOP test No. 3 to 20/345bar 5/10 min, performed BOP test No. 4 to 20/345bar 5/10 min" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed beam between slots and hatch on F-7 slot. Meanwhile lined up for BOP pressure test No. 5" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lifted spool spacer to the rig floor. Meanwhile performed BOP test No. 5, installed master bushing" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Prepared wellhead to install HP riser. Meanwhile performed BOP test No. 6, removed lifting tool for foxhole" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleared rig floor and HTS, meanwhile carried out TBT for testing BOP." "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued working on wellhead. measured RKB - WH 19.95m. Meanwhile continued pressure test on BOP. Prepared paperwork required for running HP Riser and man riding on TDS" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed communication collar. Meanwhile isolated TDS, hydraulic mech investigated sweating connection on link tilt cylinder. Finished pressure testing BOP and rigged down equipment used for pressure testing" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting to P/U high pressure riser Meanwhile deisolated TDS, TBT" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Connected all rigging equipment to TDS bails and picked up HP Riser. Removed master bushing and half-moon hatches. P/U and RIH with HP Riser, removed protector" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Continued RIH w/ HP riser, cleaned and checked seal area and M/U NT2 connector" "On 2016-08-16, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to skid BOP" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed halfmoon hatches and master bushing, released BOP NT2 connector from stump. Continued pressure testing Kill and Choke Manifold" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Skidded BOP to well center, moved port and stb tension cylinders in order to land off BOP on HP Riser Stump. Installed seal and land off BOPs. Meanwhile continued pressure testing Kill and Choke Manifold" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to connect tension cylinders. Meanwhile continued pressure testing Kill and Choke Manifold" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Connected all 4 tension cylinders to BOP carrier. Meanwhile continued pressure testing Kill and Choke Manifold" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U and run slick joint, retracted TDS. Removed master bushing and outer ring, run down and landed off slick jnt and M/U 4x studs" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U and RIH w/ diverter and land off same. Continued to M/U rest of studs on slick jnt" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to build scaffolding" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Built scaffolding around HP Riser. Meanwhile removed lifting chains from TDS. Prepared and M/U test assembly for pressure testing TDS" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Started M/U NT2 connector" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to M/U NT2 connector w/ new crew" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Finished M/U NT2 connector between BOP and riser. Meanwhile performed pressure test on TDS. Test NO.1 and Test NO. 2, Kelly hose, Upper IBOP" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed load shift from BOP carriers to tension system and pressurized diverter system. Meanwhile continued TDS pressure test. Test NO. 3, Lower IBOP" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Filled up riser and BOP with SW, closed BSR and pressure tested BOP/connector through Kill line to 20/345bar for 5/10min. Meanwhile performed TBT for rig up casing handling equipment" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U casing tong and changed BX inserts to 7inch" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U THRT and make up to first joint of the landing string" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Overtorqued connection between THRT and first joint due to wrong tong setting. Troubleshoot, broke out and inspected treads. Damaged. L/D damaged pup joint and THRT" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Broke off 2x pup joints from first landing string joint" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: P/U backup THRT and first landing string joint" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: L/D back up THRT due to it not being able to communicate with DHSV" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Prepared to P/U primary landing string. Meanwhile perform maintenance on BOP control system" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: P/U primary THRT, broke off damaged pup joint and L/D same. Replaced with new pup joint and M/U to THRT" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: P/U primary landing string" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U 3x pup joints and M/U to THRT, RIH to 22m" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH landing string to surface. Prepared and connected control lines to THRT" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH with THRT and landed on the tubing. M/U THRT to TH" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for pumping open ME plug" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Dropped 2in ball inside landing string and M/U swedge with 1502 weco to 7in tubing" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Lined up to line test. Go to low pressure 20bar. Cement pump tripped. Troubleshoot. Meanwhile lift remaining tubing handling equipment to rig floor. Reel and compact spider slips" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued w/ line test. Meanwhile prepared rigfloor for second reel" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Connected cement hose to pumping swedge and applied 20 bar to confirm line up. Continued to pressure up to 60 bar (unable to stop at 50 bar due to pressure building up to fast), no indication of opening of the Pump-open sub in ME plug. Bled off. Waited 5 min to let plug reset. Note: Plug supposed to open at 40 bar." "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressured up well to 50 bar w/ cement unit. Did not observe signs of Pump-open sub in ME plug openning . Bled off pressure via choke Meanwhile: - Called and consulted Interwell duty support. Agreed to pump up to 100bar to try to open plug. - Continued to rig up reels." "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Started to pressured up well with constant rate of 50 l/min. Observed clear change of pressure trend at 56 bar indicating openning of Pump-open sub in ME plug Stopped pressuring up at 102 bar" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Bled off pressure and monitor well on fully closed choke, no pressure build up." "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Pressured up well to equalize and open DHSV, applied 130 bar to string, observed DHSV equalizing and opening at 122bar. Pressured up control lines to 520 bar. Bled off tubing pressure to zero via choke to trip tank. Returns 60 liters indicating that DHSV closed after pressure above is pled off. Repeated equalizing and bleeding off sequence and observed same volume bled off" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Confirmed 520 bar on control line and applied 140 bar to the well, 170 liters pumped and 90 liters returned. Meanwhile evaluated situation. Discussed situation w/ onshore organisation." "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Applied 100 bar to tubing. Disconnected cement hose and bled off directly into a drum. 51 liters returned indicating that DHSV was closed" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Reconnected cement hose to tubing. Meanwhile held TBT to swap hydraulic pump to pressure up control line for DHSV" "On 2016-08-17, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Connected another hydraulic pump to control line, applied 520bar to control line. Started pressuring up tubing while monitoring gauge on the hydraulic pump for indications of DHSV sleeve movement. Observed DHSV equalized and opened at 146 bar and stop pressuring up at 152bar. No indication of DHSV sleeve movement. Bled off pressure, volume returned 60 liters. 152bar trapped below DHSV" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation, callled well integrity duty Meanwhile prepared papers and serviced/drops checked rig floor equipment" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Continued discussing way forward. Discussed risks, barrier status, well control contingencies. Agreed to attempt to pull tubing hanger with 152bar trapped pressure below DHSV. Updated change log. Meanwhile applied 20 bar to tubing and inflow tested DHSV, Good. Continued with rig maintenance and pressure tested valves S1 and C26, good" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for pulling tubing hanger as per agreed new plan" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: R/D cementing hose, chiksans. Attempted to back off weco1502 swedge. Collar backing off together with swedge. Torqued up collar to 15000 ft*lbs and manage to break off swedge, L/D same" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed circulating swedge for TDS. M/U TDS and unlock tubing hanger. Pull tubing hanger free with 185t hook load (15ton overpull). Observed drop in Trip tank indicating that A-annulus was not 100% full. Waited for trip tank level to stabilize, total of 2 m3 lost" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued to pull landing string to TH. After pulling further 9m, observed gain in trip tank indicating seals pulled out of PBR. Stopped and flowchecked, after 270l gain trip tank static. Gain volume corresponded to expected volume value due to trapped pressure below DHSV" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D THRT and to POOH 7in tubing w/ control lines" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2962m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Cut control lines. L/D TH and THRT + 2 pup joints from 2976m to 2962m" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2951m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Connected control lines to reel. Removed master bushing and installed compact spider slips. Pull 1x joint while doing adjustment on slips and tong" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2737m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Pull 7in tubing from liner 2951m to 2737m. Measured radioactivity every 10 joints. Average pulling speed 6,8joints/hour" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2737m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed time out for safety w/ crew due to radioactivity recorded in 7in tubing. 10-16 Bq/cm2 and 1-2uSv/h recorded" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2473m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued to pull 7in tubing from 2737 to 2473m. DHSV assy in rotary. Average pulling speed 10joints/hour Continued to measure radioactivity at 9-12 Bq/cm2 and 1-2uSv/h on inside of tubing and 3-4 Bq/cm2 and 0.5uSv/h on the outside of the tubing" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2473m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D Compact spider, install master bushing" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2473m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U 1x joint and cut control line to avoid having control line across BOP during WL operation. RIH w/ same and L/D DHSV" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lifted WL equipment and tool string to rig floor. Meanwhile cleaned and cleared rig floor" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U WL equipment" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: R/U for WL and M/U logging tool string (run#9). Performed surface check prior to RIH" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: RIH with logging BHA on WL. From surface to 2960m. Checked pick up weights every 500m. Average running speed 28m/min" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Logged USIT across interval 2960 - 2506 m. Performed repeat pass across interval 2960 - 2860 m. Processed and uploaded data into Interact system. Confirmed quality of data with logging duty. Received confirmation from logging duty that following intervals had high cement quality: 2895-2960m, 2660-2671m" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH from 2500 m to surface. Average pulling speed 42 m/min." "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/D WL equipment and change elevator inserts to 5,5in DP. Meanwhile function tested DHSV on deck. Observed indication of sleeve moving and flapper openning/closing" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D tubing tong" "On 2016-08-18, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: R/D tubing tong" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21s. Run down 1st std, observed back flow while running down" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U and M/U 2x 5,5in pup joints for space out" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2962m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Continued RIH with 5,5in DP from 2521m to 2962m restricted due to back flow. Performed D1 kick drill" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2962m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: M/U TDS and staged up pump rate to 3700 l/min - 178 bar. Observed increase in gas returns to 10%, stopped pump and lined up returns through gas traps" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2962m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Continued circulating with 2200 l/min - 65 bar, max gas 28% and 7ppm H2S in fluid. Circulated until gas dropped to 3% and zero H2S. Pumped through dump line with 2200 l/min to check clear." "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2962m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U and M/U pumping assembly, connected cement hose and 2x lo-torqs. Meanwhile held TBT for cementing job" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2965m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Positioned string at 2965m, lined up and pumped 20 m3 wash pill. 3700l/min - 180bar" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2965m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Lined up to cement hose and performed connection test w/ 345 bar for 3 mins. Bled off pressure to 20 bar, closed IBOP and applied 20 bar behind. Open to cement hose and verified line up" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2965m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Balanced cement plug (2965 m - 2765 m ): Mixed and pumped 9,2 m3 of 1,9 SG cement slurry, 550 l/min. Displaced the cement to the rig floor with 2900 l of drill water. Zeroed volume counters. Displaced the cement with 44 m3 (1986 strokes) of SW, 3700 l/min/ 147 bar. Pulled out of cement to 2765m at 4 min/stand. Theoretical TOC 2765 m MD." "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2765m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Installed sponge ball. Pumped 10m3 hi-vis at 1350l/min / 35 bar. Circulated 3000 l/min/ 100 bar. Meanwhile removed PS21 slips and installed master bushing. Held TBT for P/U BOP wash tool" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2722m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH and R/B 1x stand from 2765m to 2722m" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2722m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Installed closed FOSV and BOP wash tool, make 10x passes in BOP and well head at 1500 LPM / 11 bar, operated rams and annular once" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2722m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/B stand and L/D wash tool and FOSV" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2475m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH from 2722 m to 2475 m" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2475m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to rig up casing tong" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2475m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed casing tong and removed X-over" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2463m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled 1x joint of 7in tubing from 2475m to 2463m , removed master bushing and installed compact spider slips" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2463m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting pull and L/D tubing w/ control lines" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2463m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Connected control line to reel" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2415m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled 7in tubing from 2463m to 2415m. Control line jammed into slips segment, lifted slips to release Measured second joint for radioactivity at 10-30 Bq/cm2 and 1-2uSv/h on inside and 8-11 Bq/cm2 and 0.5 uSv/h on outside" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2189m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Continued pulling 7in tubing from 2415m to 2189m. Measuring for radioactivity 1-2 uSv/h on inside of tubing. Average pulling speed 11 joints/hour" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2189m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed TOFS due to finger injury to floor man. Discussed what happened and preventative measures" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1877m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Continued to pull 7in tubing from 2189m to 1877. Average pulling speed 12 joints/hour. Last joint laid down #111" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1877m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D casing handling equipment" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1877m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled up 1x joint, cut and secured control line to avoid having control line in BOP during R/D. R/D compact spider, installed master bushing. Run down and set manual slips" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1877m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D casing tongs" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1877m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U spear assembly (run#11), greased pack off, grapple and set in catch" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 1905m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH from 1876m to 1905m. Removed FOSV from liner swedge. Removed master bushings and installed PS21" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2356m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Continued RIH on 5,5in DP from 1905m to 2356m. Average running speed 450m/hour" "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2356m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: Observed loose stand in derrick. Held TBT, recovered stand using forward PRS and returned to TDS. Held stand w/ aft PRS to lower down TDS to be able to inspect elevators. Elevators found to be damaged. Changed out elevators to spare set. Performed drops check of aft PRS before continuing with operation." "On 2016-08-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2712m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Continued RIH from 2356m to 2712m. Average running speed 350 m/hour" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2768m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: M/U TDS and pumped w/ 400 l/min - 3.5 bar, 550 l/m - 5 bar. Up/down weights 202t/126t. Washed down w/ 550 l/min from 2712m to 2768m" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 899m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Tagged cement at 2768m w/ 10t, released spear by rotating 2x turns clockwise and observed torque dropped to 6kNm then increased to 9kNm. Observed hook load dropped to 90t. RIH slowly and located top of 7in tubing 7m lower or at 2775m. Set down 10t to repeat tagging of the cement" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: Dropped drift and POOH w/ spear on 5,5in DP from 899 m to surface. Avg. tripping speed 730 m/hr Retrieved drift" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled spear on surface. Inspected same, ok" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed PS21s and installed master bushings" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U MS-T seal retrieval tool" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U MS-T seal retrieval tool to 1x joint and 1x pup joint of 5,5in DP" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled MS-T seal retrieval tool to surface and connected control lines, function tested tool" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ MS-T seal retrieval tool and positioned tool stem in correct space out. Meanwhile bled off 5 bar from B-annulus." "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Turned string counter clockwise using chain tongs, only able to get 1x turn. Backed out and attempted again, 1x turn only. Tried to turn w/ iron roughneck, no go" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH and inspected tool, no damage found, observed some minor scratches" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D MS-T seal retrieval tool on HTS" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U and M/U jetting tool assembly to 5,5in DP stand" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Jetted WH area with 2200 l/min - 60bar - 10 rpm" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D wash tool and R/B DP stand" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U MS-T retrieval tool assy" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: RIH with MS-T seal retrieval tool. Rotated tool 4x turns counter clockwise to engage tool to seal. Released seal assembly w/ 80t overpull" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH w/ MS-T seal retrieval tool, removed seal assy.Disconnected control lines. L/D tool and landing string" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U cutter BHA (run#14)" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U premade cutter BHA (run#14), M/U to 5,5in DP and RIH to cutting depth of 124m" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: M/U TDS to string, checked and verified depth, filled pipe. Established parameters. 300 l/min - 30bar, 500l/min - 83bar, 100rpm, 1-5 kNm (pumps off), Weights: 73t - up, 69t - down, 70t - rotation" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cut 10 3/4in surface tie-back at 124m. 80rpm, 300 l/min - 30bar. Observed shock on surface indicating successful cut" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH w/ cutter BHA (run#14) to surface and L/D same" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Serviced drilling equipment" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U spear assembly (run#15)" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U spear assembly (run#15) from derrick, checked and serviced same" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH and latched on to 10 3/4in tie-back. Pulled free same w/ 8t overpull" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: R/U casing tong for 10 3/4in csg" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Set slips on fish and released spear. R/B spear in derrick" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Changed to BX3 elevators" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Installed elevator on hanger. Broke off and L/D same" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: POOH 10 3/4in csg tie-back from 104m to surface" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/D casing tong. Cleaned and cleared rig floor" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U torque tool BHA (run#16)" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U torque tool to 3m. Removed FOSV from swedge" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U 1x stand of 5,5in HWDP and M/U to X-over, RIH w/ 5,5in HWDP from 3m to 117m. Torqued all connections to 67500 kNm" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U TDS to 5,5in DP, RIH to 140m, started pumping with 1450 l/m, rotated w/ 10rpm. Jetted tie-back adapter area" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Stopped pumping and engaged to tie-back adapter at 141,5m. Attempted to back out Tie back adapter with 30k kNm, string backed out at Saver sub. M/U Saver sub to 50 kNm. Tried to break again up 40kNm, something broke below rotary table, after 2 turns measured distance travelled up of string +/-1in. Continued turning out further 4 turns, distance travelled further +/-2in. Assumed as good indication of Tie back adapter loose." "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH from 141,5m, visually checked all connections. When reached end of last 5,5in HWDP stand observed no BHA. The connection backed out from X-over" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH with 5,5in HWDP to fish BHA, from surface to 113m. M/U TDS to 5,5in DP and tagged top of fish at 138,5m. Rotate to screw into the fish, string stalled out at 6kNm" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH w/ BHA to surface, removed and inspect x-over, ok" "On 2016-08-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U to X-over. All connections M/U to 67kNm, Saver sub M/U to 50kNm. RIH to 117m" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued to RIH w/ torque tool to 117m" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: M/U TDS and RIH, engaged to tie-back adapter. Marked pipe. Attempted to back out adapter counter clockwise. Broke at 39kNm. Measured distance 1,5in after 5 turns. Suspected broken at connection. M/U back to 1kNm. POOH, visually checked every connection. Observed connection above X-over broke." "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Cleaned X-over connection and M/U to HWDP without applying pipe dope. All connections M/U to 67kNm, Saver sub M/U to 50kNm. RIH, engaged to tie-back adapter. Marked pipe. Attempted to back out adapter counter clockwise. Broke at +/-39kNm. Measured distance 1,5in after 5 turns. Suspected at connection. M/U back to 1kNm. POOH, visually checked every connection. Observed connection above X-over broke." "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Cleaned X-over connection and M/U to HWDP to 74kNM without applying pipe dope. All DP connections M/U to 67kNm, Saver sub M/U to 50kNm. RIH, engaged to tie-back adapter. Marked pipe. Attempted to back out adapter counter clockwise. Broke at +/-39kNm. Observed Saver sub connection broke. M/U saver sub again to 50kNm and attempted to break. Observed Saver sub connection broke." "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U manual tong and held TBT for use of manual tongs" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Trapped 20 kNm in with shaft and applied TDS break. Put tong on and pulled 20 kNm, released brake and pulled with tong to 25k n/m. Applied TDS brake. Pulled up to max 30kNm with Rig tong, observed torq reduced on TDS Shaft. Took off Rig tong, rotated TDS counter clockwise to make sure free. Made string back up to 2kNm. POOH, visually checked all connections. No connections have been observed backed out" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Started RIH w/ torque tool" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Carried out weekly HSE drill, table top exercise regarding volumetric well control" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued RIH w/ torque tool. Engaged to tie-back adapter. Marked pipe. Attempted to back out adapter counter clockwise. Applied 25kNm in steps before pipe started to rotate. Than rotated free at 2kNm. Measured distance 1,5in after 5 turns. POOH. Observed no torque tool/X/over on the drill pipe - left in hole" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH w/ DP from surface to 137 m. M/U TDS and latched on to fish. POOH from to surface. L/D torque tool" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U Left hand Tie-back adapter torque tool and M/U to X/O" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH torque tool on 5,5in left hand DP. From surface to 140. P/U singles from cantilever" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Left hand X-over arrived on the rig. Inspected and discovered it was right hand X-over. Evaluated situation. Meanwhile performed hydraulic test on BX4." "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U 1x more joint of DP and M/U to string. Attempted to break off Tie-Back adapter using rig tongs on DP. Pulled +/- 28kNm. Cathead fully stroked out. No success" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Evaluated situation. Meanwhile performed tests on Aft iron roughneck" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH from 140m to surface. L/D torque tool. Clean and clear rig floor" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U drill collars from deck" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: P/U and RIH 8,25 DC from surface to 90m (9 joints). R/B same in derrick" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U guns" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: R/U to run guns" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: P/U and M/U TCP gun BHA from surface to 17m" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to handle guns w/ new crew" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Continued to M/U guns BHA to 18m" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: RIH w/ guns on 5,5in DP to 138m" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: M/U TDS and positioned guns at 151.7m, closed UPRs and applied 20 bar to IBOP, opened to confirm line up. Up/down weights 72t/68t, flushed ball seat with 222 l/min. Opened UPRs, broke out connection and dropped 1 3/8in ball. M/U connection and positioned guns at firing depth 144,5-147,5m (top-bottom shot), closed UPRs and lined up through fully open Choke" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Pumped down ball with 160 l/min, sheared ball seat at 150 bar. Indication of guns firing (sound, vibration on surface). Top shot at 144,5m, bottom shot at 147,5m. Continued pumping with 150 l/min until returns, increased to 770 l/min, observed slight gain of 500ltr and then losses of 60m3/hr. Pumped 1,5 times btms up, gas observed and still on losses" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Stopped pumping, left choke open and opened UPRs, observed increase in flow. Close UPRs and closed choke, monitored for pressure on chole. Initially 1 bar, slowly increased to 2.9 bar then leveled out. Opened choke and slowly bled off pressure to 1 bar, closed choke and monitored for pressure build up, ok, no build up observed" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.2 hours. Operational details: Opened choke and circulateed with UPRs closed with 760 l/min, initially observed 60m3/hr losses. After confirmed returns increased flow rate to 890 l/min - 2,5 bar, max gas of 4.3%. Continued circulating until gas content curve showed downward trend. Total losses since punch 21m3" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Stopped pumping and flowchecked through fully open choke, static. Opened UPRs and flowchecked on trip tanks, static" "On 2016-08-21, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Started POOH from 147m" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: POOH w/ guns from 147m to surface" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: L/D perforation guns BHA. All shots fired" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U cutter BHA" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U and M/U cutter BHA" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: RIH w/ cutter BHA on 5,5in DP from 9,2m to 892m. Average running speed 510 m/hour. Filled pipe at 1330l/min, 3 bar" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: M/U TDS. Positioned cutters to cutting depth of 887m. Up/down weights 97t/90t, took parameters 75rpm - 4-7kNM, 300l/min - 18bar, 400l/min - 35bar, 500l/min - 61bar. Cut csg at 887m w/ 300l/min - 21bar, 80rpm - 8-12kNm. Measured gap of more than 2.7m" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: Flowchecked well. Observed instant gain of 300l, then loss of 3m3/hour. Then losses went to 0. Observed bubbling inside drill string and in the riser, smell of gas. M/U TDS to string and observed increase in trip tank" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Closed UPR and started to circulate via fully open rig choke, performed 1x full circulation at 600-1000l/min max 6bar. Stopped pump and monitor via sample line. No flow" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Opened UPR , line up trip tank and flow checked" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: POOH w/ cutting BHA on 5,5in DP from 887 m to 6 m . Avg. tripping speed 705 m/hr." "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed PS21 and installed master bushing" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: L/D cutting BHA. Cleaned and cleared rig floor" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to M/U LH landing string for torque tool" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U 1x joint of 5,5in LH DP, M/U to x-over and 1x pup joint, L/D same onto HTS. P/U and M/U tieback adapter torque tool to LH DP, RIH to 140m" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U LH DP with x-over and pup joint, M/U TDS, engaged to tieback adapter. Applied 30 kNm clockwise torque to string and released brake in an attempt to shock tieback adapter free. No success" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to use rig tongs" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Applied 25kNm counterclockwise torque with TDS and applied brake. Latched onto pipe with rig tong and pulled to max 50kNm, observed connection above x-over broke out" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting w/ oncoming crew" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Broke out TDS from pup joint and layed out joint, x-over and pup onto HTS" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Evaluated situation. Meanwhile cleaned and cleared drill floor" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Broke out pup joint from x-over, cleaned threads and M/U dry back to x-over to 67 kNm" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U joint, x-over and pup joint and M/U same to string at well center" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: M/U TDS and trapped 25kNm in string, latched rig tong and pulled to 42kNm then slowly increased to 52kNm" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for changes in the plan" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.0 hours. Operational details: Attached ropes to rig tong, trapped 26kNm with TDS. Pulled w/ rig tong up to 75kNm on the string. Tieback adapter did not release. Meanwhile discussed with onshore organization way forward" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH tieback adapter torque tool from 140 meter to surface. L/D same" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Discussed way forward. Meanwhile performed drops check on TDS and serviced same. Troubleshoot on XP pilot pressure on BX elevator." "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Started preparing milling BHA. Meanwhile continued to Troubleshoot on XP pilot pressure on BX-elevator" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: M/U milling BHA. L/D same" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U cutter assembly" "On 2016-08-22, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for change in plans" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Broke connection above the cutter. Changed and adjusted knives to 12,25in size" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: M/U cutter BHA together w/ torque tool for spaceout verification. Remeasured BHA components and pups/DP below torque tool" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ cutter BHA. Engaged torque tool in tieback adapter, P/U 21.44m up to position knives at cutting depth of 139,7m (ca middle of tieback adapter)" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: Took parameters 300l/min - 22bar, 400l/min - 49bar, 500l/min - 85bar. Cut tieback adapter at 139,7m w/ 300l/min - 19bar, 80rpm - 2-8kNm. As pressure decreased, increased pump rate to 400l/min - 7bar, 460l/min - 5bar, 530l/min - 2bar. This pressure drop indicated that knives fully retracted and tieback adapter cut" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH w/ cutting BHA" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: L/D cutting BHA" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U fishing BHA (run#21)" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH on 5,5in DP to 128 meter and latched on to 10 3/4in tieback fish" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Attempted to pull up to 80t overpull, worked the string several times up/down. No success" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH with spear BHA on 5,5in DP f/ 129m to 27m" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/B spear BHA (run#21)" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: P/U torque tool and cutter assembly (run#22) and 1x joint of 5,5in DP, M/U to TDS. Tested knives with 300 l/min, ok. Broke out TDS, continued M/U BHA to 29m" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: RIH w/ 5,5in DP and tagged top of Tie back adapter with 2T at 124m. Filled string. Evaluated new cutting depth" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Broke out TDS and POOH with cutter BHA (run#22). Installed lifting nubbing and pulled out cutter BHA" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: Changed knives in cutter to 13,5in ones. M/U TDS and tested cutter knives w/ 310 l/min, ok" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: RIH w/ 5,5DP and tagged top of Tie back adapter with 2T at 124m. Filled string and broke circulation w/ 310 l/min - 19 bar" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Positioned knives at 139.7m. Increased flow rate to 500 l/min - 82 bar, started rotating w/ 100rpm, started cutting tieback adapter w/ 1-9kNm - 60 bar, increased to 140rpm - 1-7kNm, 495 l/min - 27bar, then 600l/min - 17bar. Good indication of cut, lifted fish on knives, then pumps off" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH w/ cutter BHA (run#22)." "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: L/D torque tool and cutter BHA (run#22)" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U Spear BHA (run#23), set spear in catch position. RIH to 26m" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ spear to 106m. M/U TDS, took up/down weights 73t/70t. Continued in hole and latched onto fish at 128.5m, pulled free with 3t overpull" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Broke-out TDS and POOH w/ spear BHA. Observed fish on spear. Released spear and L/D fish, R/B spear" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U milling BHA (run#24)" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Carried out PMs and dailys while waiting for crew change helicopters" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: P/U and M/U milling BHA (run#24). RIH same to 98m" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting w/ oncoming crew" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: RIH w/ milling BHA (run#24) from 98 to 135m" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Took up/down weights 85t/82t, parameters: 80rpm - 1-5kNm, 2000l/min - 14bar" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 3.2 hours. Operational details: RIH and tagged tieback adapter cut at 139,7m, marked milling distance on pipe. P/U, started pumping and rotation 2000l/min - 13bar - 80rpm. RIH and started milling tieback adapter. Torque 2-7kNm, WOB 1t. Observed almost no vibration in the start and very noticeable vibration effects in the end of milling period. Totally milled ca 14cm down" "On 2016-08-23, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Investigated water leak on TDS" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.2 hours. Operational details: Identified leak on the wash pipe, re-tighten wash pipe, performed drops inspection on TDS. Put on hydraulic power and discovered hydraulic leak: loose connection from one of the hoses on TDS. Repaired leak." "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Resumed milling. 2000l/min - 13bar - 80rpm. Observed noticeable vibration" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Observed leak on TDS. Stopped milling. Repaired leak on the wash pipe" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 4.5 hours. Operational details: Resumed milling w/ reduced rpm. 2000l/min - 13bar - 60rpm. Observed noticeable vibration. Increased pump rate to 2500l/min - 20bar, 4-7kNm, WOB 1-3t. Totally milled 27cm down" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Stopped milling and P/U off bottom due to leaking Pod on BOPs. Found and repaired leak in hard pipe for gauge" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.5 hours. Operational details: Resumed milling 60rpm - 2500l/min - 20bar, 2-10kNm, WOB 1-3t" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Held time out for safety meeting due to first aid incident on pipe deck" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.2 hours. Operational details: Continued milling 60rpm - 2500l/min - 21bar, 4-9kNm, WOB 5-10t. Observed WOB decreased, indicating that casing hanger was milled through. Totally milled 44cm including tieback adapter part" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: P/U and stopped rotation, RIH and tagged csg stump with 5T at 144m, marked pipe" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Dressed off csg stump w/ 80rpm - 1-6kNm - 2500 l/min - 16 bar, WOB - 3t, milled down 10 cm" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Stopped rotation and P/U of bottom. Circulated 2x btms up with 3000 l/min" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: Carried out drops check of TDS and BOPs. Found loose solenoid valve on TDS, fixed and made safe. Meanwhile function tested BOPs" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: POOH w/ milling BHA from 146m to 78m" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D milling BHA (run#24)" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.2 hours. Operational details: R/B 2x stands 8,25in DC. L/D X-over. Cleaned magnets - 14,7kg of metal swarf recovered from magnet, Observed no 9,5in tapered mill in the bottom of BHA, lost in the well. Inspected pilot mill, tungstein carbide teeth almost worn out. Undergauged of 1/8in. L/D rest of BHA." "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U spear BHA. Meanwhile tested shear rams: to close - 23s/31,2gal, to open - 20s/29,8gal" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U and M/U spear BHA (run#25). Rearranged the12in stab above 8,25in DC to be able to engage spear below perforations in 10 3/4in csg" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 152m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH w/ spear assy on 5,5in DP to 152m. Weight Up/Down: 74t/71 t" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Engage spear into the fish. Pulled csg fish free w/ 50t overpull" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min" "On 2016-08-24, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Started POOH w/ csg fish on spear" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH w/ csg fish on spear. Set fish in slips. Released spear and R/B same" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U csg handling equipment" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: R/U handling equipment for 10 3/4in casing" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull and L/D casing" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 410m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 4.2 hours. Operational details: Pull 10 3/4in casing from 730m to 410m. Average pulling speed 6,5 joints/hour, max pulling speed 9 joints/hour. Pulled 28joints totally" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting w/ new crew" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: Continued pulling 10 3/4in casing from 410m to 150m. Average pulling speed 13,3 joints/hour. Pulled 48 joints totally" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Pulled FMS and installed master bushing due to low string weight" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: Continued to pull 10 3/4in casing from 150m to surface using manual slips and dog collar. Average pulling speed 8 joints/hour. Pulled totally 63 joints" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Recovered last joint and discovered tapered mill stuck in the cut, photographed and secured prior to laying out" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D casing handling equipment" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/D casing handling equipment" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: Performed drop check and greased FWD PRS, no findings. Performed drop check and greased AFT PRS, no findings" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U EZSV/cutter assembly (run#27)" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: P/U and RIH EZSV/cutter assembly (run#27) to 14.7m" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 175m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued RIH w/ EZSV/cutter assembly (run#27) to 175m. Run carefully through wellhead/casing hanger area" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 175m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and installed PS21" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Contiuned RIH from 175m to 854m. Restricted RIH speed to 2min/std" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 879m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: M/U TDS and run down to 879m, filled pipe. Washed setting area with 300 l/min - 16 bar, set EZSV at 879m mid packer depth, tagged EZSV with 10t" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 869m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Positioned cutter knives at 869m" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 869m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Recorded parameters: 309 l/min - 18 bar, 100rpm, 1-7kNm. Cut 14in casing w/ 100rpm, 310l/min. Observed pressure drop and confirmed cut window of 20cm" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 869m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Lined up to trip tank and flowchecked well. Static" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 54m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: POOH w/ EZSV running tool/cutter BHA (run#27) from 873m to 54m. Pulling wet using mud backet. Meanwhile carried out kick drill" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Retrieved drift, flow checked well. Meanwhile held prejob meeting to L/D EZSV running tool/cutting BHA (run#27)" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed PS 21, installed master bushing" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: R/B last santd of drill pipe, L/D BHA. Cleared rig floor and prepared for running guns" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U perforation guns (run#28)" "On 2016-08-25, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.8 hours. Operational details: P/U and M/U gun assembly to 18 m" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 149m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: RIH w/ perforating BHA to 149,3 m (Top shot @146 m)" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 149m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to fire guns and circulate gas" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 149m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Closed UPR, lined up to pump through choke and MGS, circulated w/ 300l/min - 0 Bar" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 149m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Broke TDS, dropped 1 3/8in ball . M/U TDS. Took up/down weights: 72t/69t. Closed UPR. Pumped down ball w/ 160 l/min, pressured up to 135 bar to shear ball seat. Good indication of guns firing. Top shot @146 m, bottom shot @149m" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 149m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Continued circulating w/ 160 l/min until stable returnes observed. Increased pump rate to 1000 l/min - 3,5bar. Max gas 3,6 % - H2S 1 ppm (in fluid). Circulated 3,5x bottoms up" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 149m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Flowchecked well through the choke. Ok. Opened UPR and flowchecked well. Ok" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: POOH w/ perforating BHA from 149m" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: L/D perforating BHA" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed handling equipment and prepared to P/U EZSV plug" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U EZSV" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: P/U EZSV plug and RT" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 834m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: RIH w/ EZSV (run# 29) to 854 mMD. Average running speed 556 m/hr." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: Established circulation and washed the setting area, 500 lpm/ 0,3 bar. Installed the 14' EZSV mechanical plug at 854 mMD. Load tested the plug with 10 ton." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 645m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 854 m to 645 mMD . Avg. tripping speed 418 m/hr." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 645m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Changed inserts in BX elevator to 5' and P/U RTTS plug. Removed PS-21 slips and installed master bushing. Changed inserts in BX elevator back to 5 1/2'" "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 788m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH w/ RTTS and safety joint on 5 1/2' DP from 645 m to 788 m (RTTS plug depth at 143.6m). RTTS plug hung up at 143.6m. Pulled up and re-attempted to RIH. Unable to run RTTS plug past restriction in WH." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 788m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Evaluated situation. Meanwhile: Greased and checked dies on IRN." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 645m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH w/ RTTS on 5 1/2' DP from 788 m to 645 m." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 645m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Changed BX inserts to 5'. L/D the RTTS and safety joint." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 648m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U 3m pup for space out. Pulled master bushing and installed PS-21 slips." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: RIH w/ EZSV RT on 5 1/2' DP from 648 m to 854 m . Avg. tripping speed 275 m/hr. Tagged EZSV w/ 2 ton to confirm depth." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U and M/U pump-in sub. Stung into EZSV and set down 10 ton. Connected cement hose and installed lo-torque valve to pump-in sub." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Closed UPR Lined up and pumped 10m3 push pill at 1000lpm / 12 bar. Circulated SW at 1000-1800 lpm / 12 bar until clean returns. Meanwhile: Performed TBT for cement job." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Opened UPR and flow checked well, static." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Lined up and pumped 20m3 wash pill at 1285 lpm / 11.5 bar. Closed upper FOSV and trapped 20 bar behind. Applied 20 bar from cement unit to drill floor and confirmed line-up. Pumped 33 m3 1.90sg cement slurry at 600 lpm. Added well-life to the first 10m3 of cement slurry (11 kg/m3). Chased cement by pumping SW at 1000 lpm / 12 bar. After catching up with cement, continued displacing cement with SW at 1000 lpm / 12 bar, then reduced rate to 800 lpm the last 1.7m3. Pumped totally 11.7m3 SW. Pressure increased from 12 bar to 47 bar, indicating that cement entered annulus. Recorded 1.8m3 losses during displacement. Estimated TOC in annulus at 480 mMD." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 854m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Released from EZSV plug and rigged down cement hose. L/D pump-in sub." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 811m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 854 m to 811 m. Installed pup joint w/ pre-loaded sponge ball. Circulated with 3450 lpm / 31 bar until clean returns. Measured 10% gas, reduced rate to 1980 lpm." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 647m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 811 m to 647 m. Avg. tripping speed 219 m/hr." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 644m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: L/D 3m pup joint." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 644 m to surface. Avg. tripping speed 970 m/hr." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed PS-21 slips and installed master bushing. L/D EZSV RT." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor." "On 2016-08-26, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.0 hours. Operational details: WOC Meanwhile: Maintenance - Replaced alignment cylinders on TDS - Performed PM inspection on drawworks - Performed PM check on FWD PRS" "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 7.0 hours. Operational details: WOC Meanwhile: Performed maintenance - Inspected flowline cover - Performed maintenance and housekeeping in pump room and shakers - Flushed chiksan hoses on WH - Continued PMs on TDS - Prepared and started to check out points on skidding checklist - Prepared tools to N/D BOP" "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: WOC De-isolated drawworks, TDS and both PRSs. Meanwhile: Prepared equipment and tools required to N/D BOP. DFO prepared pits for injection." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.2 hours. Operational details: WOC Carried out maintenance on TDS. Changed out alignment cylinder and aligned TDS to well center. Visually checked both PRSs for damages on hydraulic hoses and performed general inspection. Meanwhile: Continued with skidding checklist and prepared equipment required for next well." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: P/U and M/U EZSV RT." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: RIH w/ EZSV RT on 5 1/2' DP from surface to 42 m." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 764m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: RIH w/ EZSV RT on 5 1/2' DP from 42 m to 764 m . Avg. tripping speed 481 m/hr." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 804m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 4.0 hours. Operational details: M/U TDS sub and positioned string at 804 m. Lined up to cement unit and confirmed line-up. Attempted to pressure test annulus cement and EZSV plug to 115 bar / 10 min. Pressure had decreasing trend due to possible air in the system. Attempted to pressure up well 6 times. Less pressure drop observed for each attempt. Pressure tested annulus cement and EZSV plug to 115 bar / 10 min, bled off pressure. Meanwhile: B/O pup joints previously used for space out." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 852m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for placing cement plug in 14' casing Meanwhile: Performed line-test." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 852m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Circulated 1 x B/U at 3300 lpm / 100 bar. Max 2,5 ppm HC concentration in return fluid." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 852m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 10m3 wash pill. Mixed and pumped 8,2 m3 1,93sg cement slurry at 600 lpm. Displaced cement with cement unit by pumping 8 m3 FW (1m3 underdisplacement) at 1200 lpm." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 852m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.4 hours. Operational details: L/O pump-in sub." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 852m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.1 hours. Operational details: Flow checked well, static." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 644m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 852 m to 644 m. Restricted pulling speed 2 min/std." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 644m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Circulated 1 x string volume prior to installing sponge ball due to backflow. R/B 1 std and M/U pup joint with pre-installed sponge ball. Circulated 1 x B/U, 50 rpm / 2-4 kNm, 1200 lpm / 1 bar. L/O pup joint." "On 2016-08-27, at Well NO 15/9-F-12, a drilling event occurred at a depth of 413m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 644 m to 413 m. Avg. tripping speed 924 m/hr." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 2m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Continued POOH w/ EZSV RT on 5 1/2' DP from 413 m to 2 m. Avg. tripping speed 987 m/hr." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: L/D EZSV RT. Pulled PS-21 slips and installed master bushing" "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Cleaned and cleared drill floor. Meanwhile: Started to drain riser" "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U handling equipment for pulling diverter. Prepared to pull diverter" "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/D diverter and BOP" "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed tension cylinders on BOP" "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Removed master bushing and outer ring. Installed lifting eyes for diverter. Attempted to pull diverter, 7 ton overpull. Installed shims for releasing the diverter lock ring. Re-attempted to pull diverter. Installed tension cylinders and aligned BOP/slick joint with diverter." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing drilling crew." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Prepared to pull diverter. Removed 2 x shims from diverter housing." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed well controll table-top at drill floor." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Pulled diverter and secured to 5 1/2' DP in set-back. Removed slick joint from BOP. Disconnected BOP tension cylinders." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Broke NT2 connector. Performed TBT for skidding BOP onto test stump." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Picked up BOP using BOP carrier. Skidded BOP and landed on stump. M/U NT2 bolt." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed scaffolding around riser." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling riser." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Attached lifting arrangement to TDS bails. P/U 3 ton over pull on HP riser." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Loosened bolts on HP riser connector. 2 bolts stuck." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Worked on loosening bolts on HP riser connector. Meanwhile: Completed skidding checklist. Loosened bolts on hatch on well F-7. Installed kill wing manifold on XT on F-5." "On 2016-08-28, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Pulled and L/O HP riser. Prepared hatches in moonpool. Installed hatch on well F-12. P/U hatch on F-7 (swapping hatches between F-7 and F-9 for later operations). Meanwhile: Installed check valve in cement head. ********* End of report **********" "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding operations" "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Removed access stairs to cantilever Skidded cantilever to well F-12." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Installed access stairs to cantilever Meanwhile: Removed hatches." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Built scaffolding around hatches. Installed hole covers on well F-14" "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lowered NT2 connector from drill floor. M/U same onto multibowl. Meanwhile: Installed master bushing and BX-elevator." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for M/U BHA and RIH with inner string." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U and RIH with cutter BHA" "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U Multibowl RT. RIH and engaged RT to Multibowl. Confirmed by pulling 20 ton overpull." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Load shifted weight from tension cylinders to TDS. Meanwhile: Performed TBT for R/D tension cylinders" "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D tension cylinders" "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed boat collision stool and centralizers." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Built scaffolding around hole opening." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled 20 ton overpull. Increased flow in steps to 2600 lpm / 87 bar. Cut riser. Observed loss of overpull, good indication of cut." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D hoses and valve outlets from Multibowl." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser and inner string to drill floor. Installed C-plate and landed off riser. R/B Multibowl RT" "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed false rotary. Pulled and R/B inner string. R/B cutter BHA." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U Multibowl RT. R/D C-plate." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled tensioner joint above rotary table. Landed off riser onto elevator." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U cutting machine Cut tensioner joint. Significant wave height 1,2 m R/D cutting machine." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/O Multibowl and tensioner joint." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O Mutlibowl and tensioner joint (Lift #1). Removed Multibowl and NT2 connector." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled upper pup joint and splash zone joint. Cleaned off marine growth on centralizer deck." "On 2016-10-19, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 1,4 m" "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cutting machine" "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O upper pup and splash zone joint (Lift #2) Pulled riser (Lift #3)." "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 1 m. R/D cutting machine" "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #3). Pulled riser (Lift #4), cleaned off marine growth on centralizer deck. Riser out of splash zone at 01:45" "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #4). Pulled riser (Lift #5), cleaned off marine growth on centralizer deck." "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #5). Pulled riser (Lift #6), cleaned off marine growth on centralizer deck." "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O riser joint (Lift #6). Pulled out with lower pup joint and stress joint (Lift #7). Installed master bushing. L/O lower pup and stress joint." "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor for excess equipment." "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Cleared WH decks for excess equipment. Meanwhile: Performed skidding checks." "On 2016-10-20, at Well NO 15/9-F-12, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed hatch in moonpool **** END OF REPORT ****" "On 2009-01-13, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3401m. The activity was categorized as 'drilling -- drill' and lasted for 11.8 hours. Operational details: Drilled 8½' hole from 3210m to 3401m. Drilling parameters: Flow 2140 lpm / SPP 142-157 bars / String RPM 130 TQ 15-20 kNm / WOB 3-8,5 / ECD 1.42 EMW / MUD weight 1.34 SG / ROP 20-30 mph." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3416m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued drilling 8½' hole from 3400m to 3416m. Drilling parameters: Flow 2140 lpm / SPP 157 bars / String RPM 130 TQ 16-20 kNm / WOB 4-9 / ECD 1.42 EMW / MUD weight 1.34 SG / ROP 30 mph." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3416m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Circulated hole clean prior to take pressure points, reciprocating the string. Simultaneously held tool box talk prior to take pressure points." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3416m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed sticky test. 5min PU 192 MT SO 136 MT. 10min PU 195 MT SO 136 MT" "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3416m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Correlation log from 3416m to 3411m. Took pressure points: MD probe TVD Reservoir press. Mud hydrostatic Pressure gradient 3378m 2933.5m No test 3377m 2932.8m 297.7 bars 385.5 bars 1.035 SG 3374m 2930.9m 297.8 bars 385.3 bars 1.036 SG 3370.5m 2928.7m No test" "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3473m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued drilling 8½' hole from 3416m to 3473m. Drilling parameters: Flow 2140 lpm / SPP 156 bars / String RPM 130 TQ 17-18 kNm / WOB 2-7 / ECD 1.42 EMW / MUD weight 1.34 SG / ROP 30 mph." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3497m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 8½' BHA hole from 3473m to 3497m (TD). Drilling parameters: Flow 2140 lpm / SPP 156 bars / String RPM 130 TQ 17-18 kNm / WOB 2-7 / ECD 1.42 EMW / MUD weight 1.34 SG / ROP 30 mph." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3497m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.2 hours. Operational details: Circulated well clean reciprocating drill string 3000lpm, 140 rpm and 254 bars." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3497m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well - well static. Simultaneously held tool box talk prior to POOH pumping." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: POOH with 8½' BHA pumping from 3497m to 2531m, 1000lpm 25-40 bars. Pulling speed 203 m/hours. Leak in Kelly hose connection." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Held tool box talk prior to repair the Kelly hose. Greased auto slips, installed TIW . Cleared and cleaned the rig floor. Circulated over the T/T." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 2.8 hours. Operational details: Repaired the Kelly hose, O-ring bursted changed out same." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held tool box talk prior to slip and cut drill line." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 3.2 hours. Operational details: Slip and cut drill line." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held tool box talk prior to POOH with 8½' BHA. Simultaneously pumped 3.9m³ 1.60 SG slug." "On 2009-01-14, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2210m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: POOH with 8½' BHA on 5½' DP from 2531m to 2210m. Pulling speed 458 m/hours. Filled trip tank." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1197m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued POOH with 8½' BHA from 2210m to 1197m. Pulling speed 810 m/hours." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1197m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Changed over to 5' handling equipment." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued POOH with 8½' BHA on 5' DP from 1197m to 139m. Pulling speed 846 m/hours." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well - well static. Simultaneously held tool box talk prior to pull out and lay out 8½ BHA." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Pulled out and laid out 8½' BHA. Laid out BHA." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Broke and laid out 8 1/2' drilling BHA." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Removed excess equipment and BHA from drillfloor. Cleaned and tidied drillfloor." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Prepared fro picking up 3 1/2' DP. Changed dies in IR. Inserted auto slips. Installed rollers and function tested HTS." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 231m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: RIH with 3 1/2' DP singles from surface to 231 m MD." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 231m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Suspended tripping temporarily for conducting weather critical lifts to cantilever. Lifted 12 1/4' drilling BHA from main deck to cantilever." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH with 3 1/2' DP singles from 231 m to 300 m MD." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 300m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed from 3 1/2' to 5' handling gear." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1033m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: RIH with 5' DP from 300 m to 1033 m MD. Reduced trippping speed due to winds in excess of 50 knots. Tripping speed 590 m/hrs." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1033m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed from 5' to 5 1/2' handling gear." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2562m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: RIH with 5 1/2' DP from 1033 m to 13 3/8' shoe depth at 2562 m MD. Tripping speed 680 m/hrs." "On 2009-01-15, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3332m. The activity was categorized as 'plug abandon -- trip' and lasted for 7.0 hours. Operational details: Made up TDS. RIH with 5 1/2' DP from 2562 m to 3332 m MD while washing down at 1500 lpm on each stand. Observed occasional hang-ups and plugging tendencies and adjusted tripping speed accordingly. Tripping/washing speed 110 m/hrs." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: RIH with 5 1/2' DP from 3332 m to 3490 m MD while washing down with 1500 lpm on each stand. Tripping/washing speed 126 m/ hrs." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3498m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Made up last stand to TDS. RIH and tagged TD at 3498 m MD while pumping at 1500 lpm / 83 bar SPP. Pulled back, broke and set back stand." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: Made up TDS to 5 1/2' DP. Circulated and condtioned mud. Pumped bottoms up volume at 2250 lpm / SPP 173-178 bar. Obtained MW in/out 1,35 sg+." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up cement unit to standpipe mainfold. Tested cement line against closed standpipe mainfold valve to 200 bar / 5 min - ok." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up mud pumps. Pumped 7 m3 of 1,6 sg cement spaced at 1100 lpm / SPP 50 bar. Partly displaced cement spacer to drillfloor with 2,6 m3 OBM to put ~1 m3 cement spacer behind the cement." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3490m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Mixed and pumped 9,7 m3 1,9 sg Silica cement. Pumprate 800 lpm / CUP 45-29 bar. Displaced cement line with 890 l of seawater. Lined over to mud pumps and displaced cement with 31,6 m3 1,35 OBM. Pumprate 2000 lpm / SPP 83 bar increasing to 150 bar at the end of the displacement. Rotated 30/50 rpm during cementing and displacement / torque 11 kNm." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3280m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH with 5 1/2' DP from 3490 m to 3280 m MD. Pulled 5 dry stands." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3196m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Made up TDS and pumped 1 m3 OBM to clean 3 1/2' DP. POOH with 5 1/2' DP from 3280 m to 3196 m MD. Pulled wet pipe. Inserted cleaning sponges in string." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3196m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up TDS to string. Washed and wiped string by chasing sponge balls with 2250 lpm / SPP ~170 bar. Rotated string at 120 RPM / torque ~10 kNm." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 3196m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pumped 17 m3 1,34 sg hivis / bentonite pill at 1100 lpm / SPP 40-65 bar. Displaced hivis pill by pumping 27,6 m3 1,35 sg OBM at 2000 lpm. Observed increasing SPP peaking at 160 bar, adjusted rate to 1300 lpm accordingly. Observed erratic SPP 90-130 bar." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2897m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Lined up and filled trip tanks. POOH with 5 1/2' DP from 3196 m to 2897 m MD to locate end of string for setting 2nd cement plug in open hole. Pulled wet pipe. Tripping speed 240 m/hrs." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2897m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated out excess hivis pill at 2250 lpm / SPP~170 bar. Reduced rate to 1000 lpm / SPP 49 bar towards end of circulation. Detected hivis pill in returns indicating ideal placement." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2897m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Broke TDS. Installed CST and dart in string. Made ut TDS to string. Pumped CST down string at 1000 lpm / 43 bar. Reduced flowrate to 500 lpm / 21 bar SPP when CST entered 3 1/2' DP. Observed SPP dropping to 18 bar when CST exited 3 1/2' pipe." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pulled back to 2892 m MD. Pumped 7 m3 1,65 sg cement spacer at 2250 lpm / SPP 167 bar. Chased spacer with 2,6 m3 to put 1 m3 spacer behind cement." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Lined up cement unit to standpipe.Verified line up. Mixed and pumped 11 m3 1,9 sg G-cement to put cement plug #2 in interval 2892-2692 m MD. Pumprate 800 lpm / CUP 18 bar. Displaced cement line with 890 l of seawater. Lined over to mud pumps and displaced cement with 25,1 m3 1,35 sg OBM. Pumprate 2000 lpm. Observed erratic SPP 70-120 bar during displacement. Rotated at 60 rpm / torque 10 kNm during displacement." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2690m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Pulled out of cement with 5 1/2' DP from 2892 m to 2690 m MD. Pulled 5 dry stands." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2690m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated out excess cement with OBM at 2250 lpm / SPP 163 bar." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pumped 7 m3 1,65 sg cement spacer at 2250 lpm / SPP 167 bar. Chased spacer with 2,6 m3 to put 1 m3 spacer behind cement." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2690m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Lined up cement unit to standpipe.Verified line up. Mixed and pumped 18,5 m3 2,0 sg G-cement to put cement plug #3 in interval 2692-2512 m MD. Pumprate 800 lpm / CUP ~20 bar. Displaced cement line with 890 l of seawater. Lined over to mud pumps and displaced cement with 22,5 m3 1,35 OBM. Pumprate 2000 lpm / SPP max 125 bar. Rotated at 65 rpm / torque 10 kNm during displacement." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2432m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Pulled out of cement with 5 1/2' DP from 2690 m to 2432 m MD. Pulled 6 stands of dry pipe." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2432m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Cleaned 3 1/2' DP by pumping 1 m3 OBM at 500 lpm / 19 bar SPP." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2112m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH with 5 1/2' DP from 2432 m to 2112 m MD. Pulled wet pipe. Tripping speed 320 m/hrs." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2112m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.5 hours. Operational details: Inserted 2 ea sponge balls in string. Made up TDS. Washed and wiped string by chasing sponge balls with 2500 lpm / SPP ~180 bar. Rotated string at 120 RPM / torque 3-6 kNm. Circulated bottoms up." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2112m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped 4 m3 1,60 sg slug at 1100 lpm / SPP 45 bar. Lined up trip tanks. Allowed mud level to settle." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2112m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Function tested BOP." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1033m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: POOH with 5 1/2' DP from 2112 m to 1033 m MD. Tripping speed 617 m/hrs." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1033m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Changed from 5 1/2' to 5' handling equipment." "On 2009-01-16, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 951m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH with 5' DP from 1033 m to 951 m MD. Tripping speed 328 m/hrs." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 299m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH with 5' DP from 951 m to 299 m MD. Tripping speed 870 m/hrs." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 299m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Changed from 5' to 5 1/2' handling equipment." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 299m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for laying out 3 1/2' DP singles." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: POOH with 3 1/2' DP singles from 299 m MD to surface. Laid out singles on deck. Tripping speed 133 m/hrs." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Cleared and tidied drillfloor. Changed die carriers in IR. Removed auto slips." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: Waited on weather. Winds > 40 knots - cranes down. Meanwhile changed pneumatic control valve on TDS." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 4.8 hours. Operational details: Waited on weather. Winds > 40 knots. Meanwhile worked on TDS pneumatic valve. Planned for making up BHA using PDM, HTS and rollers." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 100m. The activity was categorized as 'plug abandon -- other' and lasted for 6.0 hours. Operational details: Picked up 12 1/4' Powerdrive exceed with PDM and slings. Placed Powerdrive on rollers and rolled onto HTS. Picked up Powerdrive from HTS and hung off same in rotary. Picked up Powerpulse with PDM and slings and placed same onto roller sections. Rolled Powerpulse onto HTS. Picked up ARC with PDM. Made up ARC to Powerpulse using chaintongs while still laying on rollers/HTS. Rolled BHA onto HTS. Picked up and made up Powerpulse/ARC to Powerdrive. Picked up and made up 2 ea NMDC. Made up jar/DC stand. Made up stand of 8 1/4' DC. Installed totco ring. Made up xover to 5 1/2' HWDP." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 286m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Installed automatic slips in RT. RIH with 12 1/4' BHA on 5 1/2' HWDP from 100 m to 286 m MD." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 286m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 286 m to 609 m MD." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 609m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Filled string. Tested MWD at 2400 lpm / SPP 91 bar - ok." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 730m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 609 m to 730 m MD." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 730m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Obtained favoruable wind conditions for manriding. Serviced PRS and TDS." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1374m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA from 730 m to 1374 m MD. Tripping speed 444 m/hrs." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1374m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Set up for drifting pipe that was not wiped/cleaned after cementing." "On 2009-01-17, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1859m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 1374 m to 1859 m MD. Drifted every stand by dropping drift in derrick. Tripping speed 243 m/hrs." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1980m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 1859 m to 1980 m MD. Drifted every stand by dropping drift in derrick. Filled pipe. Winds in derrick > 60 knots. Abandoned drifting in derrick. Discussed situation. Decided to drift by installing kelly cock in the string." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2181m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed kelly cock in string and closed same. RIH with 5 stand of 5 1/2' DP from 1980 m to 2181 m MD. Filled 500 l OBM in string and dropped drift." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 1980m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with 5 stands of 5 1/2' DP from 2181 to 1980 m MD. Broke kelly cock and recovered 2 3/4' drift." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2103m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 1980 to 2103 m MD." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2440m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: Made up TDS. Washed down from 2103 m MD to 2440 m MD. Parameters : 2000 lpm / SPP~90 bar/ 30 rpm / Torque~10 kNm. No WOB." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2490m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Washed down from 2440 m to 2490 m MD. Parameters : 2000 lpm / SPP~90bar / 30 rpm / Torque 10 kNm. Tagged top of cement at 2490 m MD. Turned off pumps and stopped roatation. Load tested top of cement with 7 MT - ok." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2504m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Drilled cement in 13 3/8' casing from 2490 m to 2504 m MD. Drilling parameters : 3000 lpm / SPP~162 bar / 60 rpm / Torque 14-18 kNm / WOB 1-3 MT. Limited ROP to 5 m/hrs due to processing cement cuttings in DCI and mud displacement. Displaced from 1,35 sg to 1,25 sg OBM while drilling stand." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2562m. The activity was categorized as 'plug abandon -- other' and lasted for 5.5 hours. Operational details: Drilled cement in 13 3/8' casing from 2504 m to shoe depth at 2562 m MD. Drilling parameters : 3000 lpm / SPP~161 bar / 60 rpm / Torque 14-18 kNm / WOB 1-5 MT. Controlled ROP to 10-15 m/hrs." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2562m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Encountered problem with DCI system - excessive solids bulid up in mill tank. Picked off bottom to 2554 m MD and circulated at 500 lpm / SPP 8 bar / 15 rpm while working on DCI system." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2566m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Reamed back to 2562 m MD. Drilled 12 1/4' section from 2562 m to 2566 m MD. Drilling parameters : 3000 lpm / SPP~164 bar / 60 rpm / Torque ~18 kNm / WOB 4 MT. Controlled ROP to 20 m/hrs." "On 2009-01-18, at Well NO 15/9-F-15 B, a drilling event occurred at a depth of 2575m. The activity was categorized as 'plug abandon -- other' and lasted for 5.5 hours. Operational details: Pulled back to 2559 m MD. Downlinked powerdrive. Drilled 12 1/4' section from 2566 m to 2575 m MD. Drilling parameters : 3000 lpm / SPP~160 bar / 80 rpm / Torque~16 kNm / WOB 2-3 MT. Controlled ROP to 2 m/hrs. (time drililling). Obtained 50/50 formation/cement shows in sample at 2575 m MD. ****Transferred operations to F-15 A****" "On 2013-05-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2627m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 12 1/4' hole from 2614 m MD to 2627 m MD with 2807 liter/min, 164-168 bar, 155 rpm, 9-13 kNm, WOB 6-13 MT." "On 2013-05-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2787m. The activity was categorized as 'drilling -- drill' and lasted for 8.5 hours. Operational details: Drilled and orientated 12 1/4' hole from 2627 m MD to 2787 m MD with 3400-3800 liter/min, 170-279 bar, 240-270 rpm, 12-22 kNm, WOB 4-9 MT, ECD 1,31-132 sg EMW. Average ROP 19 meter/hour." "On 2013-05-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2855m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 12 1/4' hole from 2787 m MD to 2855 m MD with 3815-3954 liter/min, 265-278 bar, 260-300 rpm, 14-24 kNm, WOB 8-21 MT, ECD 1,31-132 sg EMW. Average ROP 11,5 meter/hour." "On 2013-05-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2917m. The activity was categorized as 'drilling -- drill' and lasted for 12.5 hours. Operational details: Drilled and orientated 12 1/4' hole from 2855 m MD to 2917 m MD with 3815-3954 liter/min, 252-261 bar, 120 rpm, 10-22 kNm, WOB 6-21 MT, ECD 1,29 sg EMW. Average ROP 5,2 meter/hour. - Decision made to POOH for bit change." "On 2013-05-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2908m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Reamed up off bottom to 2908 m MD. Sent down linked to Rips off and racked back stand." "On 2013-05-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2908m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well for 30 min - Well static" "On 2013-05-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2546m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH wet with 12 1/4' BHA on 5 1/2' DP from 2908 m MD to 2546 m MD. Average tripping speed 241 m/hr." "On 2013-05-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2546m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well for 30 min - Well Static." "On 2013-05-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 368m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 2546 m to 368 m . Average tripping speed 871 m/hr." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 286m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' BHA from 368 m to 286 m." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 286m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well for 30 min - Well static" "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 125m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP/HWDP from 286 m to 125 m." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 125m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed auto slips and installed master bushing." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 14m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 12 1/4' BHA on 6 5/8' HWDP from 125 m to 14 m.." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Plugged in and verified MWD tools. L/D mud motor, CoPilot, AutoTrack and 12 1/4' bit. Bit Gradding: 1-3-WT-N-X-1/16-LT-PA" "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and Cleared rig floor." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: P/U back-up 12 1/4' bit, AutoTrack, CoPilot, mud motor and M/U same." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Plugged in verified and switched on MWD tools." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH 12 1/4' BHA on 5 1/2' HWDP from 25 m to 247 m" "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed master bushing and installed auto slips." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2870m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP filling string every 1000 m from 247 m to 2870 m." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2870m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Filled string and recorded SCRs." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2917m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: Washed/reamed in hole from 2870 m to 2917 m with 3500 lpm, 225 bar, 20 rpm, 10-13 kNm." "On 2013-05-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3103m. The activity was categorized as 'drilling -- drill' and lasted for 8.5 hours. Operational details: Drilled and orientated 12 1/4' hole from 2917 m to 3103 with 3800 lpm, 268 bar, 100 rpm, 17-27 kNm, WOB 8-12 MT, ECD 1,30 sg EMW. Average ROP 22 meter/hour." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3197m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled and orientated 12 1/4' hole from 3103 m to section TD at 3197 m with 3800 lpm, 268 bar, 100 rpm, 17-27 kNm, WOB 8-12 MT, ECD 1,30 sg EMW. Recorded TD survey Average ROP 18 meter/hour. TD called at 05:10 hrs." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3197m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.8 hours. Operational details: Circulated hole clean 3.5 BU with 3800 lpm, 255 bar, 120 rpm, 12-20 kNm while recipricating string." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3152m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Flowchecked well for 30 min - Well Static." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3152m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Dropped pump down Gyro and pumped down same with 800 lpm, 19 bar. Confirmed tool initialized and started." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2305m. The activity was categorized as 'drilling -- trip' and lasted for 4.2 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 3152 m to 2305 m wet while recording gyro survey. Average. tripping speed 171 m/hr." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2305m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well for 30 min - Well static." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Pumped slug and POOH with 12 1/4' BHA on 5 1/2' DP from 2305 m to 247 m . Average. tripping speed 915 m/hr." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 247m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flowchecked well for 30 min - Well static Meanwhile removed auto slips and installed master bushing." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 247 m to 140 m." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Held TBT. Recover gyro tool string and L/O same." "On 2013-05-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.8 hours. Operational details: POOH 12 1/4' BHA including HWDP to surface and L/O same. L/O 6 5/8' HWDP in singles to be sent ashore due to heavy wear on threads. Bit grading: 1-2-WT-S-X-I-NO-TD" "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Serviced drilling equipment. Clean and clered rig floor." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: P/U and M/U jet sub and wearbushing retrieval tool. RIH and washed BOP cavities with 1000 lpm, 5 bar." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 188m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: RIH with wearbushing retrieval tool and engaged wearbushing with 5 MT down wight. Picked up 45 MT overpull and released wearbushing." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH and L/O wearbushing retrieval tool and dressed wellhead with 2000 lpm, 18 bar." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: R/U handling equipment for 9 5/8' casing. Note Includes shift change and weekly fire drill." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 11m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: P/U 9 5/8' shoe joint verified float function and dropped bypass baffle. M/U shoe joint and intermediate joint unable to get good make-up grath." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 11m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out and layed out intermediate joint." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: P/U back-up intermediate joint and M/U shoe joint, intermediate joints and landing collar joint. Thread locked connections." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 334m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: RIH with 53.5 ppf 9 5/8' casing from 49 m to 334 m . Filled casing every joint Average running rate 5 joints/hr. Observed shoe float switch to self filling mode." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 334m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: M/U circulation swedge and broke circulation with 200 lpm, 2 bar. Stepped up pumps from 200 lpm in increments of 600 lpm, 8.5 bar, 1000 lpm, 12 bar to 3000 lpm, 61 bar and close shoe float self filling ports." "On 2013-06-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 827m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: RIH with 53.5 ppf 9 5/8' casing from 334 m to 827 m . Filled casing every joint.. Average running rate 10 joints/hr." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1270m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 53.5 ppf 9 5/8' casing from 827 m to 1270 m . Filled casing every joint. Average running rate10 joints/hr." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2563m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Held TBT. RIH with 53.5 ppf 9 5/8' casing stands from 1270 m to 2563 m . Filled casing every stand. Average running rate 24 joints/hr." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2563m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held TBT. Changed out casing running equipment from 9 5/8' to 10 3/4'. P/U and M/U 9 5/8' X 10 3/4' X/over. Removed 9 5/8' auto slips and installed 10 3/4' and hook- up control lines. Meanwhile: Performed deck management on cantilever and removed back-up joints." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2808m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with 65.7 ppf 10 3/4' casing from 2563 m to 2808 m. Filled casing every joint. Average running rate 7 joints/hr. Unable to function horizonta tranfer system [HTS]." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2808m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Troubleshoot HTS failure." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with 65.7 ppf 10 3/4' casing from 2808 m to 3047 m. Filled casing every joint. Average running rate 8 joints/hr." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held TBT. Changed to 5 1/2' handling equipment." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: P/U and M/U 9 5/8' X 10 3/4' casing hanger." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3047m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up and removed auto slips. RIH casing hanger below rotary and installed outerring and masterbushing. Removed casing tong and cleared rig floor of any excees equipment." "On 2013-06-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3179m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 65.7 ppf 10 3/4' casing on 5 1/2' HWDP landing string from 3047 m to 3179 m. Washed down last stand with 500 lpm, 22 bar." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3179m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: P/U and M/U cement stand." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Recorded Up/Dn weight 295/195 MT and RIH with casing hanger. Sat down 7 MT marked pipe and verified landing point. Picked up 45 MT overpull and marked pipe. Slacked off weight and sat down 7 MT. Rotated pipe 1/4 HR turn and verified stem free. Picked up 3 MT overpull prior to cement job." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Broke circulation and staged up pumps to 1700 lpm, 46 bar - No Loss to formation. Meanwhile: Held TBT, pressure tested cement lines and lined up for cement job." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- other' and lasted for 3.2 hours. Operational details: Verified cement line up and pumped 27 m3 of 1.52 sg spacer with 1200 lpm, 38 bar. Mixed and pumped 16.8 m3 of 1.90 sg cement slurry 650 lpm. Displaced the cement to the rig floor with 3m3. Zeroed stroke counters and displaced the cement with 92 m3 (4152 strokes) 1.28 sg OBM, 2500 lpm 36 bar. Observed indication of losses. Slowed down pumps and displaced cement to 110 m3 (4954 strokes) with 2000 lpm, 32 bar. Slowed down pumps to 500 lpm (FCP 40 bar) and diplaced cement with calculated displacement volume plus 1/2 shoetrack volume. Total displacement volume with rig pumps 116 m3 (5227 strokes). No indication of top plug bumped. Total losses while displacement 7-9 m3." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Bleed off pressure and checked for back flow. Monitored for back flow on trip tank. Recorded 1.2 m3 back flow over a periode of 1 hr. Closed full open safety [FOSV] valve and monitored annulus on trip tank. Meanwhile: Isolated drilling equipment and performed general maintenance." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: L/D cement head and checked for back flow. Observed flow from string Closed FOSV and installed circulation swedge. Lined up surface lines to cement unit and applied 32 bar monitoring for pressure build-up. Recorded 35 bar pressure build-up to 67 bar. Pressured up to 69 bar and held back pressure." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- wait' and lasted for 7.5 hours. Operational details: Performed general rig floor maintenance and serviced drilling equipment." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Bled off pressure and monitored for pressure build-up. No pressure build-up observed." "On 2013-06-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- wait' and lasted for 5.5 hours. Operational details: Performed general rig floor maintenance and serviced drilling equipment." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- wait' and lasted for 3.0 hours. Operational details: Performed general rig floor maintenance and serviced drilling equipment." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'interruption -- wait' and lasted for 2.8 hours. Operational details: Rigged up, slipped and cut 44 m drill line. Cleaned and cleared rig floor." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held TBT. Line up cement unit, flushed and pressure tested lines to 20/250 bar for 5/10 min." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Changed test string configuration to allow csg test to be done in one operation with cement unit and switch to mud pumps for injection test. R/D surface lines and circulation swedge." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held TBT. M/U full open safety valve [FOSV], side entry sub and 5 1/2' HWDP double. Screwed in top drive and R/U surface lines. Picked up 3 MT overpull." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Flushed and pressure tested lines to 20/250 bar for 5/10 min. Tested 9 5/8' X 10 3/4' casing to 20/250 bar for 5/10 min, 1803 L pumped and returned." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held string in tension and released casing running tool with 4 3/4 left hand turns." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Spaced out and closed upper pipe ram. Lined up cement unit and performed injection test to 113 bar, 8.9/4 m3 Pumped/returned." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Bleed back pressure and open rams. Lowered string to work hiegth, and R/D surface hose, close Lotorq. valve and open FOSV." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Spaced out and closed upper pipe rams. Bullheaded 77 m3 1.10 sg brine with 1000 lpm, 112 bar." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Shot off pumps and allowed pressure to stabilize for 10 min at 98 bar. Bleed off pressure in increemnts. Bleed down from 98 bar to 79 bar, return 1.9 m3 pressure estab. at 86 bar. Bleed down to 50 bar return 1.6 m3, pressure estab. at 74 bar. Bleed down to 30 bar, return 2 m3, pressure estab. 60 bar. Bleed down to 24 bar, return 1.3 m3, pressure estab. 13 bar. Bleed down to 0 bar, return 1.2 m3 - total 8 m3 retuns." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH and M/U casing running tool with 4 right hand turns." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Sat and pressure leak tested seal assembly to 35/207 bar for 5/10 min, 482/450 Litres Pumped/returned." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked-up 45 MT overpull and pressure tested seal assembly to 20/345 bar for 5/10 min, 456/450 Litres Pumped/returned." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Released casing running tool with 4 1/2 right hand turns. POOH to surface and L/D casing running tool" "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: P/U wearbushing combination tool and jet sub. RIH and landed wear bushing with 5MT down weight. Picked up 5 MT overpull and verified wearbushing latch in. Slacked off 5 MT down weight on tool prior to BOP test." "On 2013-06-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: Displaced BOP and pressure test BOPs to 20/345 bar for 5/10 min" "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: Pressure tested BOPs to 20/345 bar for 5/10 min" "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: POOH with wearbushing running tool and L/D same." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Pressure tested blind shear rams and casing to 20/345 bar for 5/10 min" "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.5 hours. Operational details: Vacated rig floor due to exhaust fumes from production module. Monitored exhaust CO level every 15 min." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Held TBT. Flushed lines and tested standpipe to 20/400 bar for 5/10 min." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Held TBT. P/U and M/U 8 1/2' Clean Out BHA including HWDP to 156 m." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Displaced riser to 1.28 sg OBM with 1700 lpm, 35 bar." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Held TBT. RIH 8 1/2' clean out BHA from 156 m to 196 m and performed choke drill." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed masterbushing and installed auto slips." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3101m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: RIH 8 1/2' clean out BHA on 5 1/2' DP from 196 m to 3101 m, filling string every 1000 m. Average tripping speed 775 m/hr." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3128m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Washed down from 3101 m to 3128 m with 2000 lpm, 140 bar, 30 rpm, 12-15 kNm." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3135m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH and recorded weight at 3128 m with 5 MT. Drilled excess cement from 3128 m to 3135 m with 2500 lpm, 190 bar, 60 rpm, 12-15 kNm. Observed shackers overflow." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3135m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Picked of bottom and screened down shackers." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3141m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled excess cement from 3135 m to 3141 m with 2400 lpm, 140 bar, 60 rpm, 11-15 kNm." "On 2013-06-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3177m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Tagged top of cement at 3141 m. Drilled firm cement from 3141 m to 3177 m with 2400 lpm, 140 bar, 60 rpm, 11-16 kNm, WOB 10-16 MT, Average ROP 18 m/hr." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3187m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled cement from 3177 m to 3187 m with 2400 lpm, 140 bar, 60 rpm, 11-16 kNm, WOB 10-16 MT, Average ROP 20 m/hr." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked for 15 min - Well static." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2640m. The activity was categorized as 'drilling -- trip' and lasted for 4.2 hours. Operational details: Pumped out of hole with scraper assembly from 3187 m to 2640 m with 2500 lpm, 165-150 bar, 120 rpm, 9-16 kNm making tree passes on every stand racked." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2640m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked for 15 min - Well static" "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Pumped slug and POOH with 8 1/2' clan out BHA on 5 1/2' DP from 2640 m to 156 m. Average tripping speed 994 m/hr." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min - Well static Meanwhile: Removed auto slips and installed masterbushing." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH on 5 1/2' HWDP from 156 m to surface and layed out 8 1/2' clean out BHA." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Held TBT. R/U wireline equipment and M/U cement bond log [CBL] tool string." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3187m. The activity was categorized as 'drilling -- other' and lasted for 2.8 hours. Operational details: RIH CBL tool string from surface to 3187 m." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2500m. The activity was categorized as 'drilling -- other' and lasted for 3.8 hours. Operational details: POOH while logging from 3187 m to 2500 m. TOC at 2679 m." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: POOH with CBL tool string from 2500 m to surface." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: L/O CBL tool string and R/D wireline equipment." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held TBT. Changed to 5' handling equipment" "On 2013-06-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: P/U and M/U 8 1/2' rotary steerable BHA" "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: P/U and M/U 8 1/2' rotary steerable BHA" "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Plugged-in tools and attempted to verify communication - NoGo" "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Troubleshoot MWD tools. Broke connection at Flex stab and BCPM cleaned same. M/U connetion and plugged- in tools - OK" "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Held TBT. Barriered off rig floor and installed RA source." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: P/U and M/U 8 1/2' rotary steerable BHA including 5 1/2' HWDP to 186 m." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed masterbushing and installed auto slips." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' rotary steerable BHA on 5 1/2' DP from 186 m 1000 m. Average tripping speed 1628 m/hr." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Filled string with 1.28 sg OBM and shallow tested tools with 2300 lpm, 140 bar.." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Performed choke drill." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3171m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: RIH w/ith 8 1/2' rotary steerable BHA on 5 1/2' DP from 1000 m to 3171 m filling string every 1000 m. Average tripping speed 1010 m/hr. Avg." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3187m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Established washing parameters and washed down from 3171 m to 3187 m with 1800 lpm, 40 bar, 40 rpm, 12-13 kNm." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3197m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Tagged TOC at 3187 m . Drilled shoetrack and rathole from 3187 m to 3197 m with 2000 lpm, 163 bar,60 rpm, 15-19 kNm." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 3 m new formation from 3197 m to 3200 m with 2000 lpm, 163 bar,60 rpm, 15-19 kNm. Wiped through shoetrack - No restrictions recorded." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Circulated hole clean to even MW in/out of 1.28 sg." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3200m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Lined-up cement unit, flushed and tested lines. Close BOP and performed FIT to 1.65 sg EMW with 101 bar surface pressure, 866/866 litres Pumped/Returned.." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Recorded survey at 3180 m with 2000 lpm, 158 bar. Washed down and established drilling parameters." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3250m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled and orientated 8 1/2' hole from 3200 m to 3250 m with 2400 lpm, 214 bar, 1.53 sg EMW, 80-120 rpm, 22-30 kNm, WOB 8-10 MT, Average ROP 12 m/hr" "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3250m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Recorded SCRs and tared CoPilot." "On 2013-06-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3271m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3250 m to 3271 m with 2400 lpm, 214 bar, 1.53 sg EMW, 150 rpm, 22-30 kNm, WOB 8-10 MT, Average ROP 11 m/hr." "On 2013-06-08, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3345m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3271 m to 3345 m with 2400-2500 lpm, 215-225 bar, 1.54-1.56 sg EMW, 150-160 rpm, 13-19 kNm, WOB 6-10 MT, Average ROP 12 m/hr." "On 2013-06-08, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3481m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3345 m to 3481 m with 2500 lpm, 225-238 bar, 1.55-1.56 sg EMW, 160 rpm, 15-22 kNm, WOB 7-8 MT, Average ROP 23 m/hr. Top Hugin formation found at 3468 m." "On 2013-06-08, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3625m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3481 m to 3648 m with 2500 lpm, 231-238 bar, 1.55-1.56 sg EMW, 160 rpm, 17-22 kNm, WOB 5-7 MT, Average ROP 24 m/hr, Max gas 1.6 %" "On 2013-06-08, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3776m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3648 m to 3776 m with 2500 lpm, 231-238 bar, 1.55-1.56 sg EMW, 160 rpm, 17-22 kNm, WOB 5-7 MT, Average ROP 25 m/hr, Max gas 1.6 %" "On 2013-06-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3839m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled and orientated 8 1/2' hole from 3776 m to 3839 m with 2500 lpm, 235-238 bar, 1.56-1.57 sg EMW, 160 rpm, 17-22 kNm, WOB 5-7 MT, Average ROP 23 m/hr, Max gas 1.6 %" "On 2013-06-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3852m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Reduced ROP to to enable geosteering. Drilled and orientated 8 1/2' hole from 3839 m to 3852 m with 2500 lpm, 233-235 bar, 1.55-1.56 sg EMW, 160 rpm, 13-18 kNm, WOB 1-4 MT, Average ROP 4 m/hr, Max gas 0.3 %" "On 2013-06-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3919m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Reduced ROP to enable geosteering. Drilled and orientated 8 1/2' hole from 3852 m to 3919 m with 2500 lpm, 230 bar, 1.54-1.55 sg EMW, 160 rpm, 15-22 kNm, WOB 3-6 MT, Average ROP 11 m/hr, Max gas 0.1 %" "On 2013-06-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3977m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Reduced ROP to enable geosteering. Drilled and orientated 8 1/2' hole from 3919 m to 3980 m with 2500 lpm, 230 bar, 1.54-1.55 sg EMW, 160 rpm, 17-22 kNm, WOB 5-7 MT, Average ROP 12 m/hr, Max gas 0.1 %" "On 2013-06-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4141m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 3980 m to 4141 m with 2500 lpm, 235-238 bar, 1.56-1.57 sg EMW, 160 rpm, 17-22 kNm, WOB 5-7 MT, Average ROP 23 m/hr, Max gas 1.6 %" "On 2013-06-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4283m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4141 m to 4283 m with 2500 lpm, 243-245 bar, 1.56-1.57 sg EMW, 160 rpm, 18-26 kNm, WOB 4-8 MT, Average ROP 24 m/hr, Max gas 1.7 %" "On 2013-06-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4376m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4283 m to 4376 m with 2500 lpm, 240\6 bar, 1.56-1.57 sg EMW, 160 rpm, 20-32 kNm, WOB 3-6 MT, Average ROP 16 m/hr, Max gas 1.7 %" "On 2013-06-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4479m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4376 m to 4479 m with 2500 lpm, 249-252 bar, 1.56-1.57 sg EMW, 160 rpm, 20-24 kNm, WOB 5-7 MT, Average ROP 17 m/hr, Max gas 0.3 %" "On 2013-06-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4567m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4479 m to 4567 m with 2500 lpm, 257 bar, 1.57-1.58 sg EMW, 160 rpm, 22-28 kNm, WOB 3-13 MT, Average ROP 15 m/hr, Max gas 1.8 %" "On 2013-06-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4661m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 4567 m to 4661 m with 2500 lpm, 260 bar, 1.57-1.59 sg EMW, 160 rpm, 22-29 kNm, WOB 3-13 MT, Average ROP 16 m/hr, Max gas 1.7 %" "On 2013-06-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4696m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled and orientated 8 1/2' hole from 4661 m to 4696 m with 2500 lpm, 255 bar, 1.56 sg EMW, 160 rpm, 25-30 kNm, WOB 10 MT, Average ROP 8 m/hr, Max gas 0.2 %" "On 2013-06-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4696m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Troubleshoot MWD tools. Worked string and circulated with 2500 lpm, 246 bar, 160 rpm, 25 kNm." "On 2013-06-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled and orientated 8 1/2' hole from 4696 m to section TD at 4770 m with 2500 lpm, 250-255 bar, 1.56-1.57 sg EMW, 160 rpm, 25-30 kNm, WOB 7-14 MT, Average ROP 8 m/hr, Max gas 0.1 % Called TD at 17:36 hrs." "On 2013-06-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.8 hours. Operational details: Circulated hole clean with 2500 lpm, 247 bar, 160 rpm. 25-28 kNm,, 1.52 sg EMW Circulated total 5 B/U." "On 2013-06-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- pressure detection' and lasted for 1.2 hours. Operational details: Recorded roadmap torque and flow checked - Well static." "On 2013-06-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4583m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH wet from 4770 m to 4583 m. Average tripping speed 374 m/hr." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3508m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: POOH wet from 4583 m to 3508 m. Average tripping speed 331 m/hr." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3508m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.8 hours. Operational details: Re-logged section across 3468 m with 30 m/hr to compare log response, bit depth from 3508 m to 3455 m." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP wet from 3455 m to 3170 m. Average tripping speed 127 m/hr." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3170m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min- Well static" "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3170m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: Function tested BOPs" "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3170m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Recorded torque and pipe stretch for 7' liner running." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1558m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Pumped slug POOH with 8 1/2' BHA on 5 1/2' DP from 3170 m to 1558 m. Average tripping speed 1290 m/hr. Observed problem with zone management system." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1558m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Troubleshoot zone manegement system" "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP from 1558 m to 186 m. Average tripping speed 1097 m/hr." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min- Well static" "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.8 hours. Operational details: L/D 8 1/2' rotary steerable BHA including HWDP from 186 m to surface. Bit grading: 2, 4, WT, N, X, I, BT, TD" "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held TBT. R/U 7' handling equipment." "On 2013-06-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 60m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: P/U 7' shoe joint, 3 ea. intermediate joint, float collar joint and landing collar. Verified floats function." "On 2013-06-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 341m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 29 ppf 7' liner from 60 m to 341 m. Average 4 joints/hrs. Note: Slow running speed. only one casing handling equipment operator. Due to cancelled helicopters" "On 2013-06-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1418m. The activity was categorized as 'drilling -- casing' and lasted for 18.0 hours. Operational details: RIH with 29 ppf 7' liner from 341 m to 1418 m. Average 5.2 joints/hrs. L/O a total of 6 joints w/ damged treads." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1666m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: RIH with 29 ppf 7' liner from 1418 m to 1666. Average 4 joints/hrs. L/O 4 joints w/ damaged treads (Total for the run: 17)." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1666m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting prior to P/U Liner Hanger." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1666m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Changed handling equipment. P/U and M/U liner hanger. Rigged down casing equipment. Changed handling equipment to 5 1/2' drill pipe." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: RIH with 7' liner on 5 1/2' landing string from 1666m MD to 3192m MD inside casing. Average tripping speed 190 m/hr. No losses to formation." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3192m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke circulation and increased flow rate in steps to 1000 lpm and 66 bar. Circulated one liner volume with 1000 lpm and 66 bar." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3856m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 7' liner on 5 1/2' landing string from 3192m MD to 3856m MD. Average tripping speed 221 m/hr. No losses to formation." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4095m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: From 3856m MD, observed frequent tight spots corresponding with high doglegs. Ran in hole with 7' liner on 5 1/2' landing string and worked through tight spots from 3856m MD to 4095m MD. Average tripping speed 119 m/hr. No losses to formation." "On 2013-06-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4254m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 7' liner on 5 1/2' landing string from 4095m MD to 4254m MD. Average tripping speed 159 m/hr. No losses to formation." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4745m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with 7' liner on 5 1/2' landing string from 4254m MD to 4745m MD. Average tripping speed 196 m/hr. No losses to formation." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Established circulation with 250 lpm and 60 bar. Verified parameters (up / down weights) and ran in hole with 7' liner on 5 1/2' drill pipe from 4254m MD and tagged TD at 4271m MD. Meanwhile: Performed toolbox talk prior to make up cement stand." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Spaced out with liner hanger to 3100m MD, liner shoe at 4769 m MD. Made up cement head." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Attempted to establish circulation with 100 lpm. Immediately triggered electronic popoff set at 70 bar. Investigated pressure build up in cement head." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4771m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Broke out and laid down cement head and drill pipe pup. Inspected same. Meanwhile: Cleaned and tidied rig floor. Established circulation with 360 lpm and 68 bar after confirmation that both darts were still in the cement head." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Broke off top drive and picked up and made up cement head. Dressed same." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 4.8 hours. Operational details: Established circulation to 850 lpm and 87 bar in steps. Circulated 2 x open hole volume. Established rotation at 20 rpm and 25-28 kNm. Continued circulating bottoms up with 850 lpm and 87 bar." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Dropped ball and circulated same down with 500 lpm and 60 bar. Activated hanger and verified hanger set by slacking off 30MT - ok." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Sheared out ball seat by pumping with 225 bar." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Established loss free circulation with 900 lpm and 90 bar, and rotation with 20 rpm and 19-24 kNm. Circulated and conditioned mud prior to cement operation." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pressure tested surface lines to 200 bar for 10 minutes - ok." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Pumped 5 m3 of 0.8 sg base oil at 900 lpm and 15 m3 of 1.35 sg tuned spacer followed by 3 m3 0.8 sg base oil. Closed IBOP and put 30 bar above. Opened lo-torque valve and dropped dart #1 for bottom plug. Mixed and pumped 26.7m3 1.90 sg cement slurry followed by 900 liter of drill water to displace lines. Dropped dart #2. Lined over to rig pumps and displaced cement with 1.32 sg oil based mud and 900 lpm. Sheared out bottom viper plug at 220 strokes. Sheared out top viper plug at 1467 strokes. Landed bottom viper plug at 1650 strokes. Landed top viper plug at 2910 strokes. Calculated efficiency: 95.8%. Rotated with 20 rpm to 2700 strokes. Stopped rotating liner after 2700 strokes due to torque limit exceeded. Reduced pump rate to 500 lpm at 2830 strokes. Bumped top viper plug with 130 bar circulating pressure and pressured up to 270 bar for 5 minutes - ok." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Bled down pressure to 5 bar to trip tank and perform inflow test for 5 minutes - no backflow." "On 2013-06-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pulled running tool up 4.2 m . Applied 30 tonne to set liner packer." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to cement unit and verified line up. Closed upper annular and tested annulus and liner packer to 200 bar for 10 min - ok." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Stung out of PBR with liner hanger running tool by pressuring up liner to 70 bar, pulling out 5m and observed pressure drop." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Established circulation with 2000 lpm and 110 bar. Circulated out spacer and excess cement. Transferred a total of 40m3 of slops." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4770m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out and laid down cement head and racked back." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed 2 x sponge balls and circulated 2 x string volumes at 2000 lpm and 96 bar." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Pumped slug. Laid out cement stand to deck." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Attempted to pressure test well to 270 bar. Inconclusive test due to slug and air in pipe." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 620m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Pulled out of hole with liner hanger running tool on 5 1/2' drill pipe from 3100m MD to 620m MD. Average: 620 m/hr." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 620m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up 2 x single joints from deck." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 13m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Pulled out of hole with liner hanger running tool on 5 1/2' drill pipe from 620m MD to 13m. Average: 496 m/hr." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed handling equipment. Laid out liner hanger running tool to deck." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and tidied rig floor." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up and make up flushing BHA." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 167m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Picked up and made up well protector. Ran in hole to 167m MD." "On 2013-06-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 167m. The activity was categorized as 'interruption -- other' and lasted for 8.8 hours. Operational details: Troubleshot brake release failure on top drive. Closed out fault seeking on electrical control system. Meanwhlie: Performed kick drill, rigged down drifting equipment from derrick. Serviced top drive / travelling block and dolly. Inspected and serviced PS21 slips. Prepared handling equipment for next BHA. Performed general maintenance." "On 2013-06-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 167m. The activity was categorized as 'interruption -- other' and lasted for 24.0 hours. Operational details: Troubleshot brake release failure on top drive. Assembled top drive brake without hydraulic connections. Meanwhile: Prepared brine and cut weight from 1.20 sg to 1.03 sg. Inspected handrails and gates in derrick. Cleaned upper and lower shakers. Cleaned and tidied well bay area. Prepared fast line sheave for NDT inspection. Performed general maintanence." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Assembled top drive brake without hydraulic connections. Performed PDO inpection on top drive. Tested top drive." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.5 hours. Operational details: Ran in hole with flushing assembly and flushed BOP and riser with 1600 lpm and 20 rpm. Meanwhile: Performed prejob meeting prior to pick up and make up cleanout assembly." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Drained well protector and laid down same." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to performing pressure test of well against shear ram." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Lined up and pressure tested the surface lines to 270 bar for 5 minutes. Closed shear ram. Pressure tested well to 270 bar for 10 minutes - ok. Pumped a total of 2400 liters, bled 2400 liters back. Opened shear ram." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Changed handling equipment." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up and made up cleanout assembly and removed protective covering." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 729m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: Ran in hole with cleanout assembly on 3 1/2' drill pipe to 729m MD." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 729m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed flowcheck. Prepared for picking up 3 1/2' drill pipe from cantilever." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1592m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 6.5 hours. Operational details: Picked up 3 1/2' drill pipe singles and ran in hole with cleanout assembly from 729m MD to 1592m MD." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1592m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up and made up scrape assembly." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1592m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1592m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation with 1000 lpm and 170 bar and checked up and down weights." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2271m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Ran in hole with cleanout assembly from 1592m MD to 2271m MD (scrape at 630m MD)." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2271m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Scraped area from 630m MD to 660m MD with 1000 lpm, 180 bar and 40 rpm." "On 2013-06-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2834m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Ran in hole with cleanout assembly on 5 1/2' drill pipe from 2271m MD to 2834m MD." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3977m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.5 hours. Operational details: Ran in hole with cleanout assembly from 2834m MD to 3977m MD." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3977m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up and made up 10 3/4' scraper." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4650m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Ran in hole with cleanout assembly from 3977m MD to 4650m MD." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4650m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Broke circulation with 500 lpm and 77 bar. Took up and down weights. Washed down stand from 4650m MD to 4689m MD with 500 lpm and 77 bar (9 5/8' scraper at 3080m MD. Scraped area from 3080m MD to 3066m MD with 500 lpm, 75 bar, 40 rpm and 14 kNm." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4694m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Washed down stand from 4689m MD to 4694m MD with 500 lpm and 76 bar. Tagged top of PBR at 3094m MD with 2MT. Picked up and established rotation at 30rpm. Washed and polished PBR." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4694m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated 3 x liner volume at 1300 lpm and 300 bar." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4694m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Set down weight at PBR with 16MT. Observed shearing of MFCTC." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4694m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Circulated 3 x bottoms up through MFCTC valve with 3800 lpm, 292 bar, 80 rpm and 7-16 kNm." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked up drillstring from 4694m MD to 4687m MD and activated well commissioner and verified MFCTC in closed position." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Closed pipe ram and lined up to pressure test annulus through kill line. Pressure tested annulus to 70 bar - ok." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Cycled MFCTC tool to locked closed position by setting down 19MT on PBR." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Transfered mud from sandtraps to mud pits - emptied trip tanks." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Flushed surface lines with base oil." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Perform prejob meeting prior to displace drill string to base oil." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Displaced drill string to base oil at 300-1000 lpm and 90-160 bar." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Monitored pressure and well on trip tank. Confirmed well stable with drillpipe pressure 94 bar." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Activated well commissioner packer by setting down 18MT weight on PBR." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to start inflow test." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.8 hours. Operational details: Performed inflow test in steps of 30 bar from 94 bar to 4 bar. Held 4 bar for 30 minutes. Pressure increased 0.8 bar in 30 minutes - ok." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped down base oil to 90 bar from cement unit to equalize differential pressure on well commissioner packer." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Deactivated well commissioner packer. Pulled polish mill out of PBR while rotating with 10 rpm." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Isolated cement unit and bled of pressure. Bled back 8m3 base oil to trip tank." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to start displacement to 1.03 sg brine." "On 2013-06-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Displaced well through bit to 1.03 sg brine with 1000-2000 lpm and 118-235 bar." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Continued displacing well through bit to 1.03 sg brine with 1000-2000 lpm and 118-235 bar." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Opened MFCTC tool by setting down 20 bar on PBR." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: Displaced well through MFCTC to 1.03 sg bine with 2000-4000 lpm, 40-146 bar, 90 rpm and 9-18 kNm." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Operated the MFCTC to closed position. Deactivated well commissioner packer." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flushed flowlines with 1,03 sg brine." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Prepared to perform pressure test on well down pipe and kill line. Performed line test. Pressure tested well to 345 bar with 1.03 sg brine - ok." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4687m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Performed flow check for 30 minutes - well static." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4120m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: Pulled out of hole with cleanout string on 5 1/2' drill pipe from 4687m MD to 4120m MD." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4120m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Broke out and laid down 10 3/4' scraper." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2796m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.2 hours. Operational details: Pulled out of hole with cleanout string on 5 1/2' drill pipe from 4120m MD to 2796m MD." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2796m. The activity was categorized as 'interruption -- other' and lasted for 9.5 hours. Operational details: Top drive collided with stand in the pipe racking machine and bent top joint. Performed timeout for safety and inspected for damages. Aft PRS junction box damaged. Secured stand with fore PRS and parked aft PRS. Laid out stand to cantilever. Performed PDO check of derrick." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1667m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.5 hours. Operational details: Pulled out of hole with cleanout string on 5 1/2' drill pipe from 2796m MD to 1667m MD." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1667m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Broke out and laid down well commissioner and 9 5/8' scraper." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1667m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed to 3 1/2' handling equipment." "On 2013-06-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1512m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pulled out of hole with cleanout string on 3 1/2' drill pipe from 1667m MD to 1512m MD." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 165m. The activity was categorized as 'completion -- other' and lasted for 3.5 hours. Operational details: Pulled out of hole with cleanout string on 3 1/2' drill pipe from 1512m MD to 165m MD." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 165m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Displaced surface lines and manifolds to seawater." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 165m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Displaced riser to seawater from 165m MD with 2600 lpm and 59 bar." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled out of hole with cleanout string on 3 1/2' drill pipe from 156m MD. Laid down well protector to cantilever." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed to 5 1/2' handling equipment. Cleaned and tidied rig floor." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up and run Safelock plug." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 632m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Picked up and made up Safelock plug. Ran in hole with Safelock plug to 632m MD." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 632m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Established circulation and washed the setting area with 1100 lpm and 4 bar. Installed Safelock plug at 635m MD. Top of plug at 631.6m MD." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 632m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Lined up from cement unit and pressure tested Safelock plug from below to 200 bar for 10 minutes - ok. Pumped a total of 1128 liters, bled 1120 liters back." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 632m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Closed ball valve and released Safelock running tool." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 632m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Spotted 5m3 hi-visc pill on top of Safelock plug with 1800 lpm and 11 bar." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Pulled out of hole with Safelock running tool and laid out same to cantilever." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.5 hours. Operational details: Lined up from cement unit and closed shear ram. Pressure tested Safelock plug from above to 345 bar for 10 minutes - ok. Pumped a total of 779 liters, bled 767 liters back. Opened shear ram." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up and made up bullnose and wearbushing retrieval tool." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 146m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran in hole with wearbushing retrieval tool to 146m MD. Pulled wearbushing free with 46MT overpull." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 138m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Racked back one stand and jetted wellhead with 1.03 sg brine at 2000 lpm and 20 bar." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Pulled out of hole with 10 3/4' wearbushing on 5 1/2' drill pipe. Laid out wearbushing to cantilever." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to picking up lockdown assembly." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 146m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up and made up seal assembly lockdown assembly and ran in hole on 5 1/2' drill pipe to wellhead at 138m MD." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 146m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Lined up to perform pressure test from cement unit. Pressure set seal assembly lockdown assembly with 207 bar. Verified assembly set by applying 30MT overpull." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled out of hole from 138m MD. Cleaned and tidied rig floor." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to start nippling down diverter and bell nipple." "On 2013-06-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.8 hours. Operational details: Rigged up to pull diverter. Pulled diverter. Installed master bushings. Laid diverter out to cantilever. Prepared to pull bell nipple." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 11.5 hours. Operational details: Nippled down BOP and moved over to test stump." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to remove master bushings and pick up and make up claxton tool to NT-2 connector." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Removed master bushings and outer bushings. Picked up and made up claxton tool to 5 1/2' drill pipe." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Landed off claxton tool to NT-2 connector. Attached control lines and latched running tool. Recovered control lines. Verified make up by applying 5MT overpull." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Removed scaffold from around claxton tool. Meanwhile: Cleaned and tidied rig floor." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Held prejob meeting prior to rigging down tensioning system." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 6.8 hours. Operational details: Rigged down tensioning cylinders and tension ring. Meanwhile: Prepared 24' elevator, C-plate and bails on rig floor." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Removed split hatch cover from F-11. Rigged up to run guide wires to wellhead template." "On 2013-06-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Ran guide wires to seabed." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Ran guide wires to seabed and latched in place to wellhead template using ROV. Ran hot stab hydraulic connection and connected same to hot stab receptacle on riser connector using ROV." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to disconnect high pressure drilling riser." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Released high pressure drilling riser and pulled to 1 meter above wellhead housing. ROV locked hydraulic valves on high pressure drilling riser." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Rigged up to pull high pressure drilling riser. Installed spider into rotary and installed hydraulic hoses. Function tested same." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Pulled out of hole with BOP joint. Laid out BOP joint and claxton tool to cantilever." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Changed to 24' handling equipment." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Pulled riser tension joint and laid out same to cantilever." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Changed handling equipment to 5 1/2'." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Pulled riser pup and one double (#2 + #3) joint. Laid out same to cantilever." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Unable to lay double riser joint on subrack craddle. Cut bumber bar off portside. Moved double riser joint to portside." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pull double riser joint (#4 + #5) and laid out to cantilever." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting with new crew." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Disconnected flange on single joint (#6). Installed lifting nubbing and laid out to cantilever with crane." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up single riser joint (#7) and set in spider." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Disconnected guide wires with ROV. Retrieved guide wires." "On 2013-06-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Disconnected flange on riser joint #7." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed lifting nubbing on riser joint #7 and laid out to cantilever with crane." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up lower riser pup #8 and set in spider. Disconnected flange. Installed lifting nubbing and laid out to cantilever with crane." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up and laid out stressjoint and TBC (#9) to cantilever. Meanwhile: Installed guide funnel on wellhead." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed production tension contact ring on F-11 slot. Lowered annulus valves through rotary to wellhead." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Rigged up to run production riser." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to start run production riser." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Picked up tieback connector and stessjoint and set in rotary. Picked up and made up lower riser pup." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lowered production riser through rotary to test connector. Functioned tieback connector by fully stroking out. Full stroke too long, broke ROV panel." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Pulled out with tiaback connector and riser stressjoint and set in rotary. Disconnected lower riser pup and laid out to cantilever. Laid out primary riser stressjoint to cantilever." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.8 hours. Operational details: Picked up backup riser stressjoint to rotary and made up to lower riser pup." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Tested backup tieback connector." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting with new crew." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Shimmed TBC ring. Lowered riser and landed off in riser spider." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Picked up riser single #1 and positioned and landed off joint. Inspected seal surface and installed IX-14 ring. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port - ok." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up and installed flange protection fairings." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered riser and set in riser spider. Attached guide wires to clamp." "On 2013-06-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Ran guide wires to seabed and attached to wellhead template wiht ROV. Meanwhle: Installed lifting nubbing to riser single #2." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up riser single #2 and positioned and landed off joint. Inspected seal surface and installed IX-14 ring. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port - ok. Lowered riser and set in riser spider." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Picked up riser single #3 and positioned and landed off joint. Inspected seal surface and installed IX-14 ring. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port - ok. Lowered riser and set in riser spider." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up riser single #4 and positioned and landed off joint. Inspected seal surface and installed IX-14 ring. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port - ok. Lowered riser and set in riser spider." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up splash zone riser joint." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up splash zone riser joint and landed off joint. Inspected seal surface and installed IX-14 ring. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port - ok. Lowered riser and set in riser spider." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Picked up upper riser pup joint and positioned and landed off joint. Inspected seal surface and installed IX-14 ring. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port - ok. Lowered riser and set in riser spider." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up tension joint and landed off joint. Inspected seal surface and installed IX-14 ring. Made up flange connection with bolt tensioner. Pressure tested flange connection to 3000 psi through test port - ok. Lowered riser and set in riser spider." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Modified flange protector clamp straps. Installed protector clamps." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lowered riser and attached hang off plate. Locked spider and landed off weight." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed riser running tool from riser tension joint." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up and made up 5 1/2' drill pipe with riser running tool and tension riser joint. Picked up weight and removed hangoff plate." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to remove riser spider." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed riser spider. Installed outer ring and master bushings." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Made up top drive to 5 1/2' drill pipe and riser. Spaced out to install needle valve. Ensured needle valve secured for running." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Lowered riser to safe distance above riser landing guide funnel. Verified VGX ring in correct position. Lowered riser inside vertical guide. Removed riser guide funnel." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lowered hot stab to tieback connector. Installed hot stab using ROV." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Landed off tieback connector on wellhead with 15MT. Functioned valves on ROV panel to lock tieback connector." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Applied 3000 psi until stroke indicator indicated fully set." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Picked up and applied 20MT overpull to verify latched production riser." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lined up to perform pressure test of riser." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Filled riser with water using cement unit while venting through tension joint." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to perform pressure test to 20/200 bar for 5/10 minutes." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pressure tested riser to 20/200 bar for 5/10 minutes. Pumped 320 liters. Bled 320 liters back." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Opened needle valve on tension joint to drain string. Closed needle valve." "On 2013-06-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Flushed tieback connector control lines with inhibitor using the mini reel pump." "On 2013-06-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Flushed tieback connector control lines with inhibitor using the mini reel pump. Sat all valves to parking position. Recovered hot stab and guide wires to surface. Installed dummy stab in tieback connector." "On 2013-06-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 8.8 hours. Operational details: Installed riser centralizers, tension ring and tension cylinders. Meanwhile: Pressure tested BOP to 345 bar on stump. Performed pre-job meeting prior to cut and bevel the riser tension joint." "On 2013-06-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Cut the riser tension joint while holding 2-4 Ton overpull in string. Laid out cut off riser piece and riser cutting equipment. Meanwhile: Pressure tested BOP to 345 bar on stump." "On 2013-06-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Bevelled riser tension joint edge. Held pre-job / SJA meeting prior to pick up Claxton tool and BOP joint." "On 2013-06-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Picked up and sat multibowl in rotary, inspected NT2 connection, ok. Picked up surface joint / Claxton tool assembly and made up same to multibowl. Performed pick up test of assembly to 0,15 meter above deck. Picked up assembly and removed master bushings. Ran assembly through rotary. Installed master bushings. Picked up single and ran in with multibowl. Landed out multibowl." "On 2013-06-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Tested multibowl BT and FS seals. Energized plastic in uppper and lower BT seals. Meanwhile: Attempted to pressure test annular BOP on stump." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Energized multibowl slips. Performed 5 Ton overpull test, ok. Meanwhile: Pressure tested annular BOP to 20 / 345 bar on stump. Not able to obtain test. Commenced to replace annular element." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed hatches around production riser. Meanwhile: Replacing annular preventer." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed control hose reel and pump for Claxton tool on drill floor. Meanwhile: Replacing annular preventer." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Erected scaffolding around Claxton tool in moonpool. Meanwhile: Replacing annular preventer." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Attempted to disengage Claxton tool with 1500 psi on piston. Not able to release tool. Increased pressure to 1800 psi and released Claxton tool. Meanwhile: Replacing annular preventer." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held pre-job meeting. Pulled out with Claxton tool and laid down same to cantilever deck. Meanwhile: Replacing annular preventer. Worked with installation of valves and test of multibowl." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 8.5 hours. Operational details: Replaced annular preventer. Function tested annular preventer twice prior to pressure test. Pressure tested annular preventer to 30 / 345 bar - 5 / 10 minutes, test ok. Meanwhile: Worked with installation of valves and test of multibowl. Performed maintenance on TDS. Moved slick joint and diverter to drill floor. At 17:00 hrs informed PCR to shut down production on well F-12 and F-14." "On 2013-06-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Performed pre-job meeting prior to nipple up BOP. Moved BOP to well center and landed same onto riser. Made up NT2 connector. Connected tension system. Ran slick joint and made up same. At 23:15 hrs informed PCR to restart production on well F-12 and F-14." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled master bushings. Installed diverter." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Installed BX elevator and rotator. Changed handling equipment to 5 1/2'. Picked up bowl protector RT and made up same to 5 1/2' DP. RIH and installed bowl protector. POOH with RT." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.8 hours. Operational details: Picked up and RIH with annulus insert retrieval tool. Tagged and engaged annulus insert at 140,2 meter, Not able to release annulus insert. POOH with RT. Redressed RT, replaced torque pins with torque keys. Ran back in with RT and engaged same. Released annulus insert with 4000 Nm. POOH with RT and redressed same with torque pins. RIH and retrieved annulus insert. Broke out and laid down annulus RT to cantilever." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Held pre-job meeting prior to clean out run. Picked up and made up jetting sub to 5 1/2' DP. RIH with jetting sub on 5 1/2' DP from surface to 150 m. Pumped 13 m3 hi-vis pill with 500 liter/min, 4 bar. Chased pill with 4,5 m3 SW at 500 liter/min, 2,8 bar. Stopped pumping and RIH from 150 m to 170 m. Waited for pill to soak for 10 minutes. Commenced circulation with SW between 170 m - 135 m at 3000 liter/min, 26 bar, 10 rpm, 1-3 kNm. Displaced well back to 26 m3 1,03 sg inhibited brine with 3000 liter/min, 26 bar. POOH and laid down jet sub." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Strapped DP stands from derrick." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held pre-job meeting prior to retrieving bowl protector. RIH with bowl protector retrieval tool and retrieved same. POOH with bowl protector." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Performed pre-job meeting prior to rig up. Rigged up handling equipment for 10 3/4' tie-back casing." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Held pre-job meeting prior make up setting tool. Picked up and racked back adjustable surface hanger setting tool." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleaned and cleared rigfloor. Installed large head for 10 3/4' casing handling in PDM. Performed pre-job meeting prior to run 10 3/4' tie-back string." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Picked up 10 3/4' tie-back connector, inspected same, ok. Picked up and RIH with 10 3/4' tie-back string as per running tally from surface to 103 meter." "On 2013-06-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 123m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up 10 3/4' surface casing hanger assembly with adjustment sub and continued to RIH." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Tagged land off point with 3 Ton. Landed off tie-back string at 139,73 meter Rotated string with two turns to engage threads in tie-back adapter." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released riser RT and POOH with same." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Rigged down handling equipment for 10 3/4' tie-back casing and cleared rig floor. Rigged up for handling of 5 1/2' DP." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up tie-back torque tool. Meanwhile drained riser." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with tie-back connector torque tool on 5 1/2' DP. Landed and engaged torque tool in tie-back adapter at 139,26 meter. Made up tie-back connection to 13300 Nm, turned string 5 3/4 RH turns." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with tie-back connector torque tool on 5 1/2' DP." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged up handling equipment for 10 3/4' tie-back casing. Held toolbox talk." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up casing hanger landing string and RIH to top of casing hanger at 20,9 meter. Engaged CHRT with 6 left hand turns." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- other' and lasted for 2.0 hours. Operational details: Performed pre-job meeting prior to test tie-back adapter. Rigged up swedge and hose for tie-back connector test. Flushed lines and tested lines to 345 bar for 5 minutes. Pressure tested tie-back connector to 20 / 345 bar - 5 / 10 minutes. Pumped 466 liters, bled back 461 liters. Rigged down swedge and hose." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up adjustable sub setting tool and RIH with same to 28,67 m" "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 29m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Applied 133 bar, picked up 2 Ton, bleed off pressure. Turned string 13 turns and picked up with 30 Ton overpull. Continued to turn untill 9000 Nm torque achieved. Total 14 1/4 turns. Observed correct movement through annulus port on surface WH. Final tension 30 Ton." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: POOH with adjustable sub setting tool and racked back in derrick. Changed to 10 3/4' handling equipment. Made up 10 3/4' x 2002 weco swedge. Pressure tested adjustable sub internal seal to 30 / 375 bar - 5 / 10 minutes. Pumped 446 liters, bled back 446 liters. Rigged down hose and swedge. Disengaged CHRT with 6 right hand turns. POOH with CHRT from 20,89 meter to surface. Broke out and laid down CHRT to cantilever. Rigged down 10 3/4' casing handling equipment and rigged up for handling 5 1/2' DP." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Picked up 10 3/4' MS-T seal assembly RT and made up same to 5 1/2' DP double. Connected hydraulic lines to RT and flushed through same. Function tested 10 3/4' MS-T seal assembly RT. Installed MS-T seal on RT." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 10 3/4' MS-T seal assembly and landed off at 20,86 meter. Attempted to lock RT into riser. Not able to lock RT into riser due to internal hydraulic leak i RT." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: POOH with 10 3/4' MS-T seal assembly. Picked up backup 10 3/4' MS-T seal assembly RT and tested same hydraulically. Verified RT measurements. RIH with backup 10 3/4' MS-T seal assembly and landed same at 20,86 meter." "On 2013-06-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Sat MS-T seal assembly." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Tested seal assembly to 345 bar - 10 minutes through multibowl test port. POOH with 10 3/4' MS-T seal assembly RT and laid down same." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.8 hours. Operational details: Held toolbox talk. Lined up to pressure test BOP connection and shear ram against Safe lock plug. Performed pressure test to 30 / 345 bar - 5 / 10 minutes. Pumped 553 liters, bled back 553 liters." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up bowl protector RT and made up same to 5 1/2' DP. RIH and installed bowl protector at 20,45 m." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: POOH with RT." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 4.0 hours. Operational details: Rigged up, slipped and cut drill line. Calibrated drawworks after slip and cut job. Cleaned and cleared rig floor." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to retrieve Safe Lock plug." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 611m. The activity was categorized as 'completion -- other' and lasted for 3.2 hours. Operational details: Picked up Safe Lock plug RT and made up to 5 1/2' DP. RIH with Safe Lock plug RT on 5 1/2' DP from surface to 611 m with restricted speed. At 611 meter made up TDS and commenced washing down to 629 meter with 300 liter, 3 bar. Increased flow rate to 2000 liter/min, 13 bar and displaced hi-pill out of well between 629 m - 621 m. Decreased rate to 300 liter/min, 3-4 bar and washed back down to 629 meter. Continued to wash down with 150 liter/min to top of plug at 631,6 m." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 631m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Latched onto plug at 4. attempt. Sat down 20 Ton on plug, rotated string 1/2 RH turn, took 15 Ton overpull. Slacked off 2 Ton weight and applied 35 bar, observed pressure drop to 15 bar, bleed off pressure to 0 bar. Took 2 ton overpull and rotated 24 right hand turns to release plug, pulled plug free up to 627 meter. Performed flow check for 10 minutes, ok. RIH to below plug setting point to ensure plug was retrieved and free, ok." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 2.5 hours. Operational details: Held pre-job meeting prior to POOH. POOH with Safe Lock plug on 5 1/2' DP from 639 m to surface with restricted speed. Inspected Safe Lock plug and RT, laid down same to cantilever." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Cleaned and cleared rigfloor. Picked up bowl protector RT and made up same to 5 1/2' DP. RIH to 20,55 meter and attemped to retrieve bowl protector. POOH with RT only. Inspected RT and RIH to 20,55 meter and retrieved bowl protector. POOH with bowl protector." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 3.2 hours. Operational details: Pressure tested upper / lower IBOP's and kelly hose to 20 / 345 bar - 5 /10 minutes. Meanwhile: Rigged up for running 7' completion string." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Performed pre-job meeting prior to rig up tubing equipment. Changed to 7' handling gear, BX elevators, installed rotator, adjusted link tilt function. Made up kick stand and racked back in derrick. Installed 7' casing tong and tested same." "On 2013-06-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 3.2 hours. Operational details: Installed Vario spider slips and tested same. Rigged up cable drums on rigfloor and installed sheave for DHPG. Prepared completion assembly #1 and #2 on deck." "On 2013-07-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Rigged up cable drums on rigfloor and installed sheave for DHPG. Prepared completion assembly #1 and #2 on deck. Performed pre-job meeting with all involved personnel prior to run completion string." "On 2013-07-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 67m. The activity was categorized as 'completion -- completion string' and lasted for 2.5 hours. Operational details: Picked up and RIH 7' completion from surface to 67 meter. Assembly #1 with 7' perforated stem and mule shoe. Assembly #2 with pre installed EVO plug and auto fill valve. Assembly #3 with BOT Granite packer. 2 ea. plain 7' tubing joints. Assembly #4 with DHPG. 1 ea. plain 7' tubing joint." "On 2013-07-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 67m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Terminated cable to Down Hole Temperature and Pressure Gauge. Function tested DHPG." "On 2013-07-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 715m. The activity was categorized as 'completion -- completion string' and lasted for 14.8 hours. Operational details: RIH with 7' tubing from 67 m to 715 m Average running speed 4 joints/hr. Total rejected joints 2. Observed trouble with belt on HTS." "On 2013-07-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 715m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Troubleshoot on HTS belt sensor." "On 2013-07-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 913m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: RIH with 7' tubing from 715 m to 913 m Average running speed 5,5 joints/hr. Total rejected joints 2." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 971m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: RIH with 7' tubing from 913 m to 971 m Average running speed 2 joints/hr. Total rejected joints 2. Observed hydraulic leak from elevator fitting." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 971m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Replaced broken hydraulic fitting on elevator." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1232m. The activity was categorized as 'completion -- completion string' and lasted for 4.8 hours. Operational details: RIH with 7' tubing from 971 m to 1232 m Average running speed 4,5 joints/hr. Total rejected joints 3." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1232m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Held pre-job meeting. Replaced tubing elevators to improve vertical alignment of tubing." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1316m. The activity was categorized as 'completion -- completion string' and lasted for 6.2 hours. Operational details: RIH with 7' tubing from 1232 m to 1316 m Average running speed 1 joints/hr. Total rejected joints 9 High pressure cleaned and re-doped all pins and boxes." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1500m. The activity was categorized as 'completion -- completion string' and lasted for 3.5 hours. Operational details: RIH with 7' tubing from 1316 m to 1500 m Average running speed 4,5 joints/hr. Running speed reduced due continous alignment checking and optimizing. Total rejected joints 0. Held pre-job meeting prior to adjust alignment on TDS." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1500m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Adjusted TDS alignment." "On 2013-07-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2035m. The activity was categorized as 'completion -- completion string' and lasted for 6.2 hours. Operational details: RIH with 7' tubing from 1500 m to 2035 m Average running speed 7 joints/hr. Total rejected joints 0." "On 2013-07-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2589m. The activity was categorized as 'completion -- completion string' and lasted for 11.2 hours. Operational details: RIH with 7' tubing from 2035 m to 2589 m Average running speed 4 joints/hr. Total rejected joints 7." "On 2013-07-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2612m. The activity was categorized as 'completion -- completion string' and lasted for 4.2 hours. Operational details: Performed pre-job meeting prior to run DHSV. Installed sheave for DHSV control line in PRS. Picked up and made up assembly #5 DHSV and made up same to string. RIH with completion string from 2589 m to 2595 m. Installed and terminated DHSV control lines. Tested DHSV control lines to 520 bar, bled back 370 ml. Tested DHSV control lines to 345 bar and maintained DHSV open while contiue to RIH from 2595 m to 2612 m." "On 2013-07-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2612m. The activity was categorized as 'completion -- completion string' and lasted for 3.5 hours. Operational details: At 20,55 meter below rotary observed string taking 15 Ton weight. Not able to enter centralizer on assembly #5 into 10 3/4' casing in multi-bowl. Picked up string. Attempted to run through multi-bowl, still observing string taking weight. Pulled out to inspect DHSV assembly for contact marks, no marks observed. Observed rig not proper alignet above well." "On 2013-07-03, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2612m. The activity was categorized as 'completion -- other' and lasted for 5.0 hours. Operational details: Prepared for skidding rig." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2612m. The activity was categorized as 'completion -- other' and lasted for 1.5 hours. Operational details: Prepared for skidding rig. Held pre-job meeting prior to skid. Skidded rig 15 cm forward. Attempted to run through multi-bowl, still observing string taking weight. Pulled out to inspect DHSV assembly for contact marks, no marks observed. Ran back in with DHSV assembly, sat down 10 - 15 Ton weight on 10 3/4' casing stump, passed through." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2798m. The activity was categorized as 'completion -- completion string' and lasted for 3.5 hours. Operational details: RIH with 7' tubing from 2612 m to 2798 m. Average running speed 5 joints/hr. Total rejected joints 0." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2798m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Replaced elevator due to trouble with latch function." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3066m. The activity was categorized as 'completion -- completion string' and lasted for 5.0 hours. Operational details: RIH with 7' tubing from 2798 m to 3066 m. Average running speed 4,5 joints/hr." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3066m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Recorded up / down weights, 186 / 139 Ton. Changed to 5 1/2' DP elevators. Rigged down sheaves for control lines. Picked up pre-made DP landing stand and made up to tubing string. Installed masterbushings and manual slips." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Performed pre-job meeting prior to RIH. Washed down with 7' tubing on 5 1/2' DP from 3066 m to 3099,7 m at 150 liter/min, sat down 5 Ton on PBR no go. Pulled back 4,5 meter out of PBR and increased rate to 220 liter/min. Stung into PBR to confirm depth, observed small pressure peak when stinging in. Continued to RIH and confirmed depth by setting down 5 Ton onto PBR no go at 3099,7 meter." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3100m. The activity was categorized as 'completion -- completion string' and lasted for 4.5 hours. Operational details: Picked up until weight observed. Marked pipe. POOH with 7' tubing on 5 1/2' DP. Strapped pipe while POOH. Broke out landing string. Replaced box on joint 14 due to poor threads. Meanwhile: Prepared space out and picked up space out joints from cantilever." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3076m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Held pre-job meeting. Made up two space out joints and RIH from 3099,7 m to 3075,7 m." "On 2013-07-04, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3076m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Made up tubing hanger to space out joint. Fed the control lines through hanger and terminated same." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3076m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Leak tested all penetrations / fittings to 35 / 450 bar - 5 / 10 minutes, ok" "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3076m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Installed C-plate and landed tubing in same. Broke out handling tool. Wrapped control and gauge lines 4 times around hanger neck." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3076m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Connected lines to ports in communication collar. Picked up and connected tubing hanger RT to hanger with 8 LH turns. Connected DHSV control lines and tested same to 520 bar / 10 minutes. Connected tubing hanger RT control lines to GE reel. Left 520 bar in DHSV control line." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Picked up and made up landing joints to string. RIH with hanger and landed same on 7' landing string from 3075,7 m to 3098,20 m. 1,27 meter stick up. Verified correct hanger land and seal integrity by testing to 70 bar - 5 min through ports on multi-bowl. Engaged tubing hanger lock down ring. Performed pull test to 15 Ton overpull, ok. Meanwhile drained riser." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested liner hanger seal to 35 / 345 bar - 5 / 10 min. Opened DHSV." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Rigged up swedge and cement hose, tested same to 345 bar - 10 min." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Dropped ball." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Circulated ball down with 3500 liter/min, 32 bar, pressure increased to 70 bar at landing. Held 70 bar pressure for 5 min to check integrity." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Increased pressure to 345 bar and held same for 30 minutes to set packer. Meanwhile observed vent line on annulus A. Bled pressure down to 280 bar. Closed DHSV Bled pressure down to 210 bar and performed low pressure inflow test, 70 bar, 30 min. Bled pressure down to 10 bar and performed high pressure inflow test, 280 bar, 10 min. Bled pressure back to 0 bar and opened DHSV." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Lined up and tested connection from cement unit to A annulus. Performed pressure test of production packer though A annulus to 35 / 345 bar, 5 / 10 min." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3098m. The activity was categorized as 'completion -- other' and lasted for 1.2 hours. Operational details: Held pre-job meeting prior to rig up wireline equipment. Rigged up wireline sheaves and equipment. Made up wireline tool string." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 5.8 hours. Operational details: RIH with wireline tool string and retrieved EVO plug. While POOH observed stuck EVO plug inside DHG mandrel, jarred twice and continued to POOH to surface. Laid out EVO plug and wireline tool string. Rigged down wireline sheaves and equipment." "On 2013-07-05, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Pressure tested line up from cement unit to drill floor to 355 bar -10 minutes. Pressure tested production packer from below to 345 bar- 30 minutes." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pressure tested production packer from below to 345 bar- 30 minutes. Rigged down surface lines. Closed DHSV." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held pre-job meeting. Disconnected tubing hanger RT by rotating 9 turns clockwise. POOH with 7' landing string and tubing hanger, laid out same." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Rigged down tubing handling equipment. Cleaned and cleared rigfloor." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.8 hours. Operational details: Rigged up handling equipment for 3 1/2' DP. Picked up and RIH with 6 3/8' k-type BPV on 3 1/2' DP. Installed BPV and POOH with RT, laid out same." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.2 hours. Operational details: Performed pre-job meeting prior to nipple down BOP. Rigged up handling equipment for nipple job on rigfloor. Nippled down diverter, pulled same to rigfloor and secured. Removed riser tension cylinders. Disconnected BOP from HP riser and skidded same to stump. Pulled riser to rigfloor." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: Terminated contol lines on wellhead Meanwhile: Laid out HP riser onto HTS. Prepared spacer spool." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Run down with spacer spool and landed same on multi-bowl. Made up spacer spool and tested same. Meanwhile transportet scaffolding equipment up in derrick." "On 2013-07-06, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Removed A annulus test hose from wellhead deck. Installed split hatches onto riser on tensioner deck. Removed hatch from F-11. Transferred XMT from overhead crane TDS. Not able to run XMT through hatch." "On 2013-07-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed Hatch from F-6." "On 2013-07-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Ran down and landed XMT onto spool. Orientation veryfied by laser. Made up XMT to spool piece. Removed XMT lift cap and installed test cap." "On 2013-07-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 13.2 hours. Operational details: Installed hatches on well F-11 and F-6. Performed termination of control system and flowlines on XMT. Meanwhile: Replaced drill line guide. Replaced HTS belt. Changed out brake on TDS. Worked with installation of new flowline valve in shaker house. At 16:00 hrs handed over the well to Maersk Production." "On 2013-07-07, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 8.0 hours. Operational details: Erected scaffolding in derrick to enable access to aft PRS. Worked with installation of new flowline valve in shaker house. Meanwhile: Performed termination of control system and flowlines on XMT." "On 2013-07-08, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 16.5 hours. Operational details: Erected scaffolding in derrick to enable access to aft PRS. Replaced junction box aft PRS. Performed planned maintenance on TDS and BOP. Prepared to rig up wireline equipment. Meanwhile: Performed termination of control system and flowlines on XMT. At 16:30 hrs the well was handed back from Maersk Production." "On 2013-07-08, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: Held pre-job meeting. Pressure tested XMT body and associated valves to 35 / 345 bar - 5 / 10 minutes." "On 2013-07-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed XMT cap. RIH with BPV RT on tugger from rigfloor. Retrieved 6 3/8' BPV and POOH with same." "On 2013-07-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 6.2 hours. Operational details: Removed F-11 hatch Rigged up wireline BOP, riser and lubricator." "On 2013-07-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 3.0 hours. Operational details: Held pre-job meeting. Filled riser with 100% MEG. Leak tested WL rig up to 30 / 200 bar - 5 / 10 min using cement pump. Function tested WL BOP. Connected hoses to lubricator and grease injector head. Mounted slings and sheaves in TDS" "On 2013-07-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 3.2 hours. Operational details: Performed test between tractor and WL interface." "On 2013-07-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 2.0 hours. Operational details: Rigged up lower sheave. Connected tractor to wireline. Stabbed lubricator section onto riser. Pressure tested WL rig up with tractor only to 30 / 200 bar - 5 / 10 min using cement pump. Drained lubricator and broke out same." "On 2013-07-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 6.8 hours. Operational details: Performed pre-job meeting prior to handling of toolstring. Made up WL toolstring with guns and RIH. ( Tool length: 29.86m, MAX OD:4.5 in, Tool Weight:1157.65 kg) Armed the guns. Stabbed lubricator. Pressure tested In-situ sub to 30 / 200 bar - 5 / 10 min." "On 2013-07-09, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Opened well according to procedure. WHP: 80bar" "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3700m. The activity was categorized as 'completion -- perforate' and lasted for 6.0 hours. Operational details: RIH with perforate BHA #1 on WL tractor from surface to 3700 meter. Not able to pass 3700 meter with string. Push with 1000 lbs with tractor. Simulations predicted 400 lbs push." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3666m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Evaluated situation. Discussed situation with onshore organisation." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3570m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Held TBT. POOH with BHA # 1 from 3700 m to 3570 m and tested tractor." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3919m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: RIH with BHA # 1 on WL tractor from 3570 m and passed restriction at 3700 m. RIH to 3919 m. Unable to communicate with tractor." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3919m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Trouble shoot communication failure, No Go. Discussed situation with onshore organisation" "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: POOH with BHA # 1 from 3919 m to 250 m." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Held TBT. POOH with BHA # 1 from 250 m to surface." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Closed in well. Drained and broke lubricator. Broke down tool string and L/O same." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Checked wire line tools and cable. Meanwhile: Checked tractor and found communication failure due to possible short circuit." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Held TBT. P/U and M/U BHA # 1RR. Stabbed lubricator on In-Situ Sub." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Pressure tested In-Situ Sub to 30/200 bar for 5/10 min." "On 2013-07-10, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3471m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Opened well and RIH with BHA #1RR on WL from surface to 3471 m (Tool length: 29.86m, MAX OD:4.5 in, Tool Weight:1157.65 kg) WHP: 80 bar" "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3700m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: RIH with BHA # 1RR from 3470 m to 3592 m." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3700m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Engaged tractor and RIH with BHA # 1RR from 3592 m to 3700 m. ." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3700m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Unable to pass restriction at 3700 m . Attempted to work passed restriction from 3660 m to 3700 m." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3750m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Pulled back to 3300 m. RIH with BHA # 1RR on wireline from 3300 m to 3557 m. Engaged tractor and RIH with BHA # 1RR on WL tractor from 3557 m to 3750 m. Performed pick-up test and confirmed tool depth." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3919m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: RIH with BHA # 1RR on WL tractor from 3750 m to 3919 m" "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4570m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: RIH with BHA # 1RR on WL tractor from 3919 m to 4570 m" "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3900m. The activity was categorized as 'completion -- perforate' and lasted for 5.0 hours. Operational details: Performed correlation run from 4570 m to 3900 m. Observed wireline jumped spool grove." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4160m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Payed out wireline and Re-spooled to 4160 m." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4580m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Performed correlation run from 4160 m to 4580 m" "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4539m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Bleed off well head pressure from 80 bar to 39 bar. Positioned guns at perforating interval # 1 between 4539 m to 4527 m and fired guns, Good indication of guns fired. Well head pressure stabilized at 34.7 bar." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.8 hours. Operational details: POOH with perforating BHA # 1RR from 4539 m to surface. Observed wireline cable released from tool." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Closed in well on swap valve and hydraulic master valve [HMV]" "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Evaluated situation and formulated plan forward." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Inflow tested HMV with 5 bar for 10 min and purged lubricator with nitrogen." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Broke lubricator connection and secured perforating BHA # 1RR with C-plate. Picked-up and verified guns fired. Broke connection above guns and secured tool string inside lubricator and L/O same." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: POOH with gun assembly and L/O same." "On 2013-07-11, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Checked equipment and cleared rig floor" "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: Builed cablehead and function tested wireline tractor." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: R/U wireline sheave. Tested interface between wireline tractor and logging tools Voltage Protection Module and Casing Collar Locator." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Held TBT. P/U lubricator and wireline sheave." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: P/U and M/U wireline tractor to cablehead. M/U lubricator and tested tractor communication. Pressure tested In-situ sub to 30/200 bar, 5/10 min." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Displaced lubricator and pressure tested same to 30/345 bar for 5/10 min." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.8 hours. Operational details: Held TBT. Bleed off pressure and broke out lubricator. P/U and M/U perforation gun assembly #2." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator and pressure tested In-Situ Sub to 30/345 bar for 5/10 min." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Equalized wellhead pressure to 35 bar and opened well." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3360m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: RIH with perforation BHA # 2 on wireline from surface to 3360 m. (Tool length: 30.85m, MAX OD:4.5 in, Tool Weight: 1184.65 kg) WHP:34.7 bar" "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4564m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: RIH with perforation BHA # 2 on wireline tractor from 3360 m to 4564 m." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4500m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Correlated across perforation interval and positioned gun with top shot at 4500 m . WHP 33 bar." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4500m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval from 4488 m to 4500 m. Wellhead pressure stabilized at 35 bar." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.8 hours. Operational details: POOH with perforation BHA # 2 on wireline from 4500 m to surface. Closed well, inflow tested and bleed down to 0 bar." "On 2013-07-12, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Held TBT. Broke lubricator and L/O guns." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: B/O and L/O perforation BHA # 2. Layed out wireline and cut same at cablehead." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Re-Build cablehead and prepared guns for perforation run # 3." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Tested interface between wireline tractor and logging tools Voltage Protection Module and Casing Collar Locator." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Held TBT. P/U and M/U perforation BHA # 3. M/U lubricator and tested In-Situ Sub to 30/200 bar for 5/10 min. (Tool length: 30.85m, MAX OD:4.5 in, Tool Weight: 1184.65 kg)" "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4420m. The activity was categorized as 'completion -- perforate' and lasted for 5.2 hours. Operational details: RIH with perforation BHA # 3 from surface to 4420 m." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4420m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Attempted to correlate gun position for perforation interval # 3. Lost communication with perforation BHA # 3." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: POOH to surface. Closed-in well and inflow tested same. bleed off wellhead pressure to 0 bar and broke out lubricator." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: L/D BHA on cantiliver deck and troubleshoot communication failure. Communication failure identified in cablehead." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Build new cablehead and tested tools." "On 2013-07-13, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: P/U and M/U perforation BHA # 3RR." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U lubricator and tested In-Situ Sub to 30/200 bar for 5/10 min." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3470m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: RIH with perforation BHA # 3RR on wireline from surface to 3470 m. WHP 37 bar. (Tool length: 30.85m, MAX OD:4.5 in, Tool Weight: 1184.65 kg)" "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4450m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: RIH with perforation BHA # 3RR on wireline tractor from 3470 m to 4450 m." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4450m. The activity was categorized as 'completion -- perforate' and lasted for 3.2 hours. Operational details: Correlated across perforation interval # 3 and positioned guns. WHP: 39 bar" "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4367m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval # 3 from 4355 m to 4367 m. WHP stabilized at 39 bar." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.2 hours. Operational details: POOH with perforation BHA # 3RR from 4367 m to surface." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Held TBT. Closed-in well and inflow tested same. Bleed down pressure to 0 bar and broke out lubricator." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: L/O perforation BHA # 3RR." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Re-build cablehead and tested tools." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: Held TBT. P/U and M/U perforation BHA # 4 (Tool length: 27.01m, MAX OD: 4.5in, Tool Weight: 974.65 kg)" "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator and pressure tested In-Situ Sub to 30/200 bar for 5/10 min. Eqaulized pressure and opened well." "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3390m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: RIH with perforation BHA # 4 on wireline from surface to 3390 m. WHP 42 bar" "On 2013-07-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3825m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with perforation BHA # 4 on wireline tractor from 3390 m to 3825 m." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4470m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: RIH with perforation BHA # 4 on wireline tractor from 3825 m to 4470 m." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4450m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Attempted to correlate across interval # 4 from 4470 m. Lost communication with tool string at 4450 m." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.8 hours. Operational details: POOH with perforation BHA # 4 on wireline from 4450 m to surface. WHP 42 bar." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Closed-in well and inflow tested same. Bleed down pressure to 0 bar." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Broke out lubrictor and L/O tools. Wireline logging computer blacked out at 07:30 hrs." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Cut wireline and L/D lubricator. R/D wireline wench and prepared to R/U back-up wench." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Spudded back-up wench on cantilever." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Hooked-up and tested wireline unit. Installed new logging computer." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Attempted to test wireline caple, No Go. Slipped and cut 200m sections untill good test. Slipped and cut 800 m wireline and achieved good test." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Build cablehead and P/U lubricator." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: P/U and M/U wireline tractor to cablehead. Tested tractor communication and M/U lubricator." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Pressure tested In-situ sub to 30/200 bar, 5/10 min. Displaced lubricator and pressure tested same to 30/345 bar for 5/10 min." "On 2013-07-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Bleed off pressure and broke out lubricator. P/U and M/U perforation BHA # 4RR." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: P/U and M/U perforation BHA # 4RR. M/U lubricator and tested In-situ Sub to 30/300 bar for 5/10 min. (Tool length: 30.85m, MAX OD:4.5 in, Tool Weight: 1184.65 kg)" "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3400m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: RIH with perforation BHA # 4RR on wireline from surface to 3400 m. WHP 47 bar" "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3670m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: RIH with perforation BHA # 4RR on wireline tractor from 3400 m to 3670 m." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3921m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Worked assembly from 3670 m to 3921 m. Unable to pass 3921 m." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: POOH from 3921 m to surface." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.2 hours. Operational details: Closed and inflow tested well. Broke lubricator and L/O BHA # 4RR." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: L/D lubricator and changed greasehead. R/U wireline, build caplehead and tested tools." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: P/U and M/U wireline tractor and lubricator. Pressure tested In-Situ Sub to 30/300 bar for 5/10 min and Lubricator to 30/345 bar for 5/10 min." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Broke out lubricator. P/U perforation guns and M/U perforation BHA # 4RR2" "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U lubricator and tested In-Situ Sub to 30/300 bar for 5/10 min. Eqaulized pressure and opened well." "On 2013-07-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 500m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: RIH perforation BHA # 4RR2 from surface to 500 m." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3332m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: RIH with perforation BHA # 4RR2 on wireline from 500 m to 3332 m. Attempted to function Voltage Protection Module to engage tractor, No Go." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3332m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Attempted to troubleshoot communication failure, No Go." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: POOH with perforation BHA # 4RR2 on wireline from 3332 m to surface." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Closed and inflow tested Swab and Hydraulic master valves with 46 bar differential pressure. Broke out lubricator and L/O tools." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Troubleshoot tool failure. Build new cablehead and changed out Voltage Protection Moule, Power Track Advanced, swivel and tractor" "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: P/U tractor assembly and lubricator. M/U lubricator and tested tools. Eqaulized pressure and opened well. (Tool length: 30.85m, MAX OD:4.5 in, Tool Weight: 1184.65 kg) WHP: 51 bar" "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3350m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: RIH with perforation BHA # 4RR3 on wireline from surface to 3350 m. Tools tested at 250 m." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4040m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: RIH with perforation BHA # 4RR3 on wireline tractor from 3350 m to 4040 m." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4316m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Correlated and positioned gun assembly at perforation interval # 4 from 4304 m to 4316 m. WHP 51 bar" "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4316m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval # 4 from 4304 m to 4316 m, good indication of guns fired. 51 bar WHP before and after perforation." "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: POOH with perforation BHA # 4RR3 from 4316 m to surface. WHP 52 bar" "On 2013-07-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: Closed and inflow tested Swab and Hydraulic master valves with 47 bar differential pressure." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Bleed down pressure to 0 bar and broke out lubricator." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: L/O perforation BHA # 4RR3 and L/D lubricator" "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: Re-build cablehead and tested tools. Meanwhile removed topdrive pipe handler for service." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: P/U lubricator and M/U perforation BHA # 5." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: M/U lubricator and pressure tested In-Situ Sub to 30/300 bar for 5/10 min. Eqaulized pressure and opened well." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3377m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: RIH with perforation BHA # 5 on wireline from surface to 3377 m. (Tool length: 27.01m, MAX OD: 4.5in, Tool Weight: 974.65 kg)" "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4305m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: RIH with perforation BHA # 5 on wireline tractor from 3377 m to 4305 m." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4295m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Correlated and postioned gun assembly at perforation interval # 5 from 4295 m to 4286 m. WHP: 53.6 bar before and after perforation" "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4295m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval # 5, good indication of guns fired." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.0 hours. Operational details: POOH with perforation BHA # 5 from 4295 m to surface." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.2 hours. Operational details: Closed and inflow tested HMV/SWAB valve. Broke out lubricator and L/O perforation BHA # 5." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Re-biuld cablehead and tested tools. Meanwhile: Removed washpipe and checked bolts on topdrive main chaft bearing retainer." "On 2013-07-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.8 hours. Operational details: P/U lubricator and perforation BHA # 6." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: M/U perforation BHA # 6." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: M/U lubricator and pressure tested In-Situ Sub to 30/300 bar for 5/10 min. Eqaulized pressure and opened well. WHP 55 bar." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3400m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: RIH with perforation BHA # 6 on wireline from surface to 3400 m (Tool length: 30.85m, MAX OD:4.5 in, Tool Weight: 1184.65 kg) WHP: 56 bar" "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4325m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: RIH with perforation BHA # 6 on wireline tractor from 3400 m to 4325 m." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4280m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Correlated across interval # 6 from 4280 m to 4268 m and positioned guns." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4280m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval # 6 from 4268 m to 4280 m, good indication of guns fired." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.2 hours. Operational details: POOH with perforation BHA # 6 from 4280 m to surface. WHP 56 bar." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: Closed and inflow tested HMV/SWAB valve with 51 bar differential pressure." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Broke out lubricator and L/O perforation BHA # 6." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.2 hours. Operational details: Re-build cablehead and tested tools prior to P/U perforation BHA # 7." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: P/U and M/U perforation BHA # 7" "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: M/U lubricator and pressure tested In-Situ Sub to 30/300 bar for 5/10 min." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3529m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: RIH with perforation BHA # 7 on wireline from surface to 3529 m." "On 2013-07-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3693m. The activity was categorized as 'completion -- perforate' and lasted for 0.5 hours. Operational details: RIH with perforation BHA # 7 on wireline tractor from 3529 m to 3693 m." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4130m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: RIH with perforation BHA # 7 on wireline tractor from 3693 m to 4130 m" "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4075m. The activity was categorized as 'completion -- perforate' and lasted for 2.8 hours. Operational details: Correlated and positioned gun assembly at perforation interval # 7 from 4075 m to 4065 m. WHP 57.5 bar" "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4075m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval # 7, good indication of guns fired. WHP 58.1 bar (Tool length: 30.85m, MAX OD:4.5 in, Tool Weight: 1184.65 kg)" "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.2 hours. Operational details: POOH with perforation BHA # 7 from 4075 m to Surface. WHP 59 bar." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.5 hours. Operational details: Closed and inflow tested HMV/SWAB valve with 54 bar differential pressure." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Broke out lubricator and L/O perforation BHA # 7." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: Re-build cablehead and tested tools." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.0 hours. Operational details: P/U and M/U perforation BHA # 8." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.0 hours. Operational details: M/U lubricator and pressure tested In-Situ Sub to 30/300 bar for 5/10 min. Eqaulized pressure and opened well. WHP 59 bar." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4095m. The activity was categorized as 'completion -- perforate' and lasted for 4.5 hours. Operational details: RIH with perforation BHA # 8 from surface to 4095 m" "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4043m. The activity was categorized as 'completion -- perforate' and lasted for 1.2 hours. Operational details: Correlated and positioned gun assembly at perforation interval # 8." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4043m. The activity was categorized as 'completion -- perforate' and lasted for 0.2 hours. Operational details: Perforated interval # 8 from 4043 m to 4031 m." "On 2013-07-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 3.5 hours. Operational details: POOH with perforation BHA # 8 from 4043 m to surface. WHP 59 bar." "On 2013-07-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 1.8 hours. Operational details: Inflow tested surface controlled subsea safety valve for 30 min and hydraulic master valve for 10 min with 56 bar differential." "On 2013-07-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- perforate' and lasted for 2.5 hours. Operational details: Purged riser and lubricator. B/O lubricator and L/O perforation BHA # 8." "On 2013-07-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- wire line' and lasted for 6.2 hours. Operational details: R/D wireline equipment." "On 2013-07-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 12.5 hours. Operational details: Prepared for skidding operation: Installed weather deck hatches on slot F-11. Installed drilling hatches on slot F-1 R/D Enviro Unit hand rails and moved same 3 m port. Performed deck manegement in preparation of equipment for 26' section. Performed maintenance of drilling equipment. Spudded Gyro wireline equipment on cantiliver deck. L/O 26' mud motor BHA on cantiliver. ******* Reporting transfered to F-1 *********" "On 2013-07-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4769m. The activity was categorized as 'completion -- other' and lasted for 4.0 hours. Operational details: Started reporting rig activity on F-1 at 23:00hrs on 21.07.2013 Prepared for final pressure test on F-11B Xmas tree before handover to production department. Performed testing on tree as follows: - Filled Xmas tree with MEG using MEG injection pump. Pressure tested tree cap to 30/200 bar for 5/10min, good test. - Pressure tested Swab valve to 30/200 bar for 5/10 mi, good test - Bullheaded 3 m3 MEG into tubing using MEG injection pump, followed by 6,6 m3 packer fluid using cement pump and 1,2 m3 MEG with MEG injection pump. Closed DHSV and inflow tested same for 30 min, good test. Suspended further testing on F-11 tree until F-1 26' section below DHSV" "On 2013-07-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4769m. The activity was categorized as 'completion -- other' and lasted for 3.0 hours. Operational details: Continued offline pressure test operations on F-11 Xmas tree for handover to production department. - Inflow tested HMV for 10 min, good test. - Inflow tested MMV for 10 min, good test. - Installed 2' weco blind cap on KWV. - Pressured tested Xmas tree KWV cap and KWV to 35/200 bar for 5/10 min, good test. Well F-11B handed over to production 23.07.2013 at 20:00 hrs." "On 2015-10-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Vessel arrived rig. Unloaded WL equipment from vessel." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Continued to lift containers from vessel." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Spotted equipment on pipedeck according to spotting plan. Started to hook up units to power. Meanwhile spotted containers on drill floor." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Prepared cables for hookup of the general surface equipment." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held platform general alarm exercise with all crew." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 8.0 hours. Operational details: Rigged up general surface equipment; WL winch and add on, Altus and Schlumberger logging units, working containers etc. Built scaffolding around units." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Leak tested BOP to 20/345 bar for 5/10 min on stump." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Function tested BOP rams from winch panel." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Finalized WL winch and function tested same." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Lifted riser pieces to drill floor prior to start building lower riser section and lubricator. Lifted grease injection head, GIH, and prepared same. Meanwhile Altus and Schlumberger started to prepare BHA for testing." "On 2015-10-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Built lubricator horizontally using tugger and catwalk. Meanwhile built GIH." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Continued to build lubricator and installed same in elevator connected to top drive. Built lower riser section and top lubricator. Meanwhile production department started to close in well." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Spotted BOP in moonpool area. Connected GIH to top lubricator and treaded cable." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Hooked up airhose to line viper. Meanwhile Altus megged cable and built cablehead." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Spooled out hoses for BOP, test pump and hoses for HMV & DHSV down to moonpool. Meanwhile Altus megged cablehead and function tested tractor." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Connected hoses to grease injection head." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.0 hours. Operational details: Waited on production to complete shutting inn and inflow test well. Meanwhile performed toolbox talk for changing hatch and rigging up. Altus and Schlumberger tested toolstring." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Received well from production department." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Changed well hatch with wireline hatch." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Disconnected top cap and landed lower riser and BOP. Hooked up hoses and function tested same. Meanwhile Altus and Schlumberger completed string test." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Rigged up kill wing manifold, bleedoff hose and equalizing loop over to prod. wing." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Filled oil on pump for DHSV & HMV and prepared same, had some issue with air into system." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Lined up via BOP for inflow test / Leak test of swab and kill wing manifold." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for testing swab and Kill wing manifold." "On 2015-10-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Inflow tested / leak tested swab to 20/345 bar for 5/10 min according to program. Leak tested kill wing manifold and hoses to 20/345 bar for 5/10 min." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Hooked up hoses for local control of DHSV and HMV and tested same." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.2 hours. Operational details: Performed pre job meeting prior to install lubricator sections." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Lifted middle lubricator section and connected same to BOP. Lifted top lubricator." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: M/U BHA #1 Tractor and PLT/RST and installed same." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Stabbed lubricator and filled rig up with MEG using production permanent lines via XMT cross. Leak tested R/U to 20/345 bar for 5/10 min. Meanwhile performed communication check with tools." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Opened HMV. Pressurized DHSV control line. Production pumped MEG via XMT cross to equalize across DHSV and opened same." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Equalized pressure across swab and opened same." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 540m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH w/ BHA #1 (Tractor & PLT/RST) by gravity from surface to 540 m, WHP 94 bar." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 540m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Schlumberger performed communication check with toolstring." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2750m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Continued to RIH by gravity from 540 m to 2750 m. Stopped for spinner calibration. Depth PU 400 m 1150 lbs 800 m 1350 lbs 1200 m 2000 lbs 1600 m 2300 lbs 2000 m 2950 lbs 2400 m 3450 lbs FF at 0,3 or slightly below" "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2750m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Performed spinner calibration at 10, 20, 30 & 40 m/min. Meanwhile performed well control drill." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Continued to RIH by gravity. Observed tool stopped at 2800 m. PU weight 3850 lbs. Had to start tractor." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Switched over to tractor mode." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3570m. The activity was categorized as 'workover -- wire line' and lasted for 1.6 hours. Operational details: RIH using tractor from 2800 m to 3570 m. Tractor software froze." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3570m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Restarted tractor software, OK." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4530m. The activity was categorized as 'workover -- wire line' and lasted for 2.3 hours. Operational details: Continued to RIH using tractor from 3570 m to 4530 m. Stopped to perform first sigma logging pass. Depth PU 3200 m 4200 lbs 3600 m 4150 lbs 4000 m 4800 lbs 4500 m 6100 lbs FF at 0,3 or slightly below" "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3440m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Powered up minitron and started 10 m/min up pass. Logged sigma across 4530 to 3430 m." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4270m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Switched over to tractor mode and tractored back down from 3440 m to 4270 m." "On 2015-10-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4200m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Powered up RST tool to perform first IC up pass at 0,5 m/min. Logged across interval 4254 to 4200 m. WHP 102 bar." "On 2015-10-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3818m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Continued to log RST IC pass at 0,5 m/min across interval from 4200 to 4188 m, 4045 to 3895 m and 3827 up to 3818 m. Meanwhile performed well control drill." "On 2015-10-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3470m. The activity was categorized as 'workover -- wire line' and lasted for 7.2 hours. Operational details: Continued to log IC pass at 0,5 m/min from 3818 to 3660 m and 3522 to 3470 m. Completed logging first IC pass." "On 2015-10-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4270m. The activity was categorized as 'workover -- wire line' and lasted for 1.9 hours. Operational details: Switched over to tractor and tractored down from 3470 m to 4270 m." "On 2015-10-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3780m. The activity was categorized as 'workover -- wire line' and lasted for 8.9 hours. Operational details: Switched over to logging mode and started second IC pass. Logged IC pass at 0,5 m/min from 4254 to 4188 m, 4045 to 3895 m and 3827 to 3780 m. WHP 109." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3470m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Continued to log RST IC pass at 0,5 m/min from 3780 to 3660 and 3522 to 3470 m. Completed logging second IC pass." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4525m. The activity was categorized as 'workover -- wire line' and lasted for 2.4 hours. Operational details: Switched over to tractor and tractored back down to 4525 m to perform PLT shut in pass." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3994m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Switched over to logging mode and performed shut in PLT pass at 20 m/min across interval 4520 to 4000 m. Parked toolstring at 3994 m." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3994m. The activity was categorized as 'workover -- wire line' and lasted for 5.4 hours. Operational details: Petec evaluated data. RST data was good. Challenging to evaluate PLT shut in passes. Had to re-arrange wells prior to startup F-11 B for production. Production ready to open well." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3994m. The activity was categorized as 'workover -- wire line' and lasted for 0.9 hours. Operational details: Equalized pressure PWV using equalizing loop. Well routed towards HP separator. Opened choke 6%. WHP 108 bar and DHPG 302 bar." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.8 hours. Operational details: Opened choke stepwise up to 12%. WHP 59 bar and DHPG 258 bar." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Opened choke stepwise up to 20%. WHP 46 bar and DHPG 239 bar. Meanwhile observed pressure in DHSV CL was at 520 bar." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Opened choke stepwise up to 24%. WHP 43 bar and DHPG 235 bar. Meanwhile Isolated DHSV CL on wellhead and bled of pressure at pump to avoid bleeding off to 0 bar. Repeated sequence until CL pressure was 420 bar." "On 2015-10-29, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Opened choke stepwise up to 34%. WHP 38 bar and DHPG 227 bar." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3994m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Opened choke stepwise to 70 %. WHP 32 bar and DHPG 222 bar." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3994m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Opened choke stepwise to 100 %. WHP 32 bar and DHPG 222 bar." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4530m. The activity was categorized as 'workover -- wire line' and lasted for 1.6 hours. Operational details: Switched over to tractor mode and RIH to perform 1. PLT flowing pass. Observed higher pullforce on tractor headtension 600 lbs compared to 300 lbs during shut in passes. Stopped at 4530 m." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3997m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Switched over to logging mode and picked back up. Tension peaked at 9000 lbs (SLB counter) but decreased to approx. 6900 lbs. Logged PLT flowing pass at 10 m/min across interval 4520 m to 4000 m." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4530m. The activity was categorized as 'workover -- wire line' and lasted for 1.4 hours. Operational details: Switched over to tractor mode and RIH to perform 2. PLT flowing pass." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3990m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Switched over to logging mode and picked back up. Logged PLT flowing pass at 20 m/min across interval 4520 m to 4000 m." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4530m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Switched over to tractor mode and RIH to perform 3. PLT flowing pass." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3986m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Switched over to logging mode and picked back up. Logged PLT flowing pass at 30 m/min across interval 4520 m to 4000 m." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3986m. The activity was categorized as 'workover -- wire line' and lasted for 4.8 hours. Operational details: PETEC evaluated data from PLT flowing passes. Decision made to re-run one pass. Observed trouble to start tractor." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3986m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Problem with tractor power supply. Had to change power supply on surface. OK." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3986m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Decision made to not run the additional pass. PLT data was good enough for further decision. Shut in well and POOH. WHP 35 bar." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: POOH from 3986 m to surface. WHP 90 bar." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.7 hours. Operational details: Closed SV and bled off lubricator. Inflow tested SV. Closed HMV and inflow tested same, monitored pressure in XMT cross. Meanwhile purged lubricator with N2 via bleed manifold." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to L/D BHA#1." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.7 hours. Operational details: Broke lubricator. L/D BHA #1 on deck." "On 2015-10-30, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Altus and Schlumberger strated to prepare toolstring for perforation run #1." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: Altus performed communication check with tools. Not able to communicate with Altus VPM through tractor." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Restarted all surface systems and changed to different VPM sub. Communication with VPM sub OK, but not able to switch same. Reviewed issue from last campaign, not similar issue." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Contacted onshore duty and continued to troubleshoot." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Removed the additional rig-grounding on the tool and switched VPM directly from the panel. VPM was switching OK. Issue most likely related to current grounding." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Lifted tractor and assembled with Schlumberger toolstring to perform Schlumberger tool check." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Lifted tools to rig floor due to wind picking up. Continued to check tools." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Powered down tools prior to handling explosives." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to M/U BHA#2 tractor & perforation guns." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 3.0 hours. Operational details: M/U BHA #2 Tractor and perforation gun. Added 40 litres of Starlube into lubricator. Challenging to handle heavy 4,5' perforation gun. Leak tested QTS to 20/345 bar." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Filled lubricator with MEG using production permanent line into XMT cross. Equalized and opened HMV. Equalized and opened SV. WHP 118 bar. Meanwhile performed well control drill, leak in connection above BOP." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 210m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: RIH with BHA#2 Tractor and 4,5' Perforation guns from surface to 70 m below seabed." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 210m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed communications check with tractor and tools." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Continued to RIH from 210 m to 2800 m. Observed tool stopped. Had to start tractor. Depth PU (Altus winch) 400 m 2070 lbs 800 m 2630 lbs 1200 m 3100 lbs 1600 m 3800 lbs 2000 m 4150 lbs 2400 m 5050 lbs 2800 m 6000 lbs" "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4030m. The activity was categorized as 'workover -- perforate' and lasted for 4.2 hours. Operational details: Switched over to tractor. Tractored down from 2800 m to 4030 m. Observed tractor speed decreased to approx. 2-3 m/min. Depth PU (Altus winch) 3200 m 7000 lbs 3600 m 6700 lbs 4000 m 8000 lbs" "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3930m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Performed gun check, OK. Performed first correlation pass at 10 m/min from 4030 to 3930 m. Observed high pulling weighs at between 8000-9000 lbs (Schlumberger counter). Adjusted depth by +4 m." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4034m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: Switched over to tractor and tractored back down. Tractor speed approx. 2-3 m/min." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3930m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Switched over to logging. Performed second correlation pass at 10 m/min. Max tension 9800 lbs (Schlumberger counter)." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3930m. The activity was categorized as 'workover -- perforate' and lasted for 2.8 hours. Operational details: Repeated sequence and performed 3 passes between 4030 to 3930 m, to ensure perforation guns properly oriented." "On 2015-10-31, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4020m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Tractored back down prior to position guns for perforation." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3900m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Switched over to logging. Logged up from 4020 m and positioned toolstring with top shot at 3960 m. Perforated interval 3960 - 3969 m. WHP 119 bar. No indication on cable tension, DHPG increased by 0,3 bar. Logged up after shooting." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: POOH from 3900 m to 2800 m . Observed leak on grease skid." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Leak on the drum for one of the hoses running from the grease skid up to GIH. Isolated same and continued POOH with only one hose injecting grease to GIH." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.7 hours. Operational details: Continued to POOH from 2800 m to surface. When at DHSV depth performed PA announcement for handling explosives on drillfloor." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Closed SV and HMV and inflow tested same. Purged lubricator with N2." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to break lubricator and L/D toolstring." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.4 hours. Operational details: Broke lubricator and L/D BHA #2. Observed all shots fired." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 4.5 hours. Operational details: Altus and Schlumberger started tool check for next perforation toolstring. Meanwhile Altus wireline changed grease hose on GIH." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to M/U BHA#3." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.1 hours. Operational details: Installed BHA #3 tractor and 4,5' perforation guns into lubricator. Added 40 litres of Starlube into lubricator." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Stabbed lubricator and leak tested QTS to 20/345 bar for 5/10 min. Production filled lubricator with MEG using permanent line into XMT cross. Equalized and opened HMV and SV. WHP 119 bar." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 300m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: RIH w/ BHA #3 Tractor and 4,5' perforation guns from surface to 300 m." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 300m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Powered up tool and checked communication." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Continued to RIH from 300 m to 2800 m. Tool stopped. Had to start tractor." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Switched over to tractor. Observed problems with tractor communication." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Checked tractor power supply. OK. Checked all connections. Found loose connection. Communication OK." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4030m. The activity was categorized as 'workover -- perforate' and lasted for 4.1 hours. Operational details: Tractored down from 2800 m to 4030 m. Tractor speed decreased to approx. 2-4 m/min." "On 2015-11-01, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3860m. The activity was categorized as 'workover -- perforate' and lasted for 2.4 hours. Operational details: Swiched over to logging and performed first correlation pass at 10 m/min from 4030 to 3860 m. Run back in and repeated sequence for orientation of guns. Run back in with tractor." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3860m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Switched over logging and performed second orientation pass at 10 m/min from 4030 m to 3860 m." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 4020m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Switched over to tractor and RIH to position gun prior to perforate." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3918m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Switched over to logging and P/U to position for perforation. Observed log was 1 meter shallow. Repeated pass, still shallow. Shifted depth +0,7 m. Performed new pass and positioned gun. Perforated interval 3910 - 3919 m. Observed shots fired on tension. WHP 118 bar." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3853m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Logged up. Observed logging tool not communicating. Stopped and checked communication. Possible short in tool after perforation." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.5 hours. Operational details: POOH from 3853 m to surface." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.0 hours. Operational details: Closed SV & HMV and inflow tested same. Purged lubricator with N2." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to L/D BHA #3." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Broke lubricator and L/D BHA #3 on deck. All shots fired." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Latched lubricator for lifting lubricator & BOP." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 5.5 hours. Operational details: Closed BOP and opened HMV for inflow testing of DHSV. Bled off pressure above DHSV. Meanwhile held toolbox talk prior to rig down lubricator, BOP and riser from XMT." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Closed HMV and bleed off pressure below BOP." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.2 hours. Operational details: Disconnected hoses to BOP and prepared to lift rig up off XMT. Disconnected riser on XMT. Lifted lubricator, BOP and riser using top-drive and double securing, secured same in rotary." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.6 hours. Operational details: Installed top cap and leak tested XMT top cap to 20/345 bar for 5/10 min. Meanwhile prepared for skidding rig." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Had to wait due to skidding from F-11B to F-5." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.0 hours. Operational details: Installed KWV cap and leak tested same to 20/345 bar for 5/10 min." "On 2015-11-02, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Disconnected lines for local control of DHSV and HMV. Cleaned and tidyed area. Handed well over to production. ------------------------- END OF OPERATION -----------------------------" "On 2016-04-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held Pre-job meeting with night crew." "On 2016-04-14, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.5 hours. Operational details: Vessel arrived rig. Unloaded WL equipment from vessel." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Spotted equipment on pipedeck according to spotting plan. Checked and and verified all equipment recieved." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Prepared hoses and cables for hookup of surface equipment." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held pre-job meeting with day crew." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Continued to prepare equipment prior to rig up." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Started to verify equipment according to Maersk checklist for hookup to rig." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Lifted Grease injection head and toolcatcher to drillfloor. Fed cable through GIH." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Maersk electrician connected power to Altus and SLB units. Meanwhile, lifted PCE equipment to drillfloor." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held toolbox talk with involved personell prior to start building riser." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Built riser and lubricator section on catwalk using tugger. Meanwhile, finalized and function tested WL winch. Schlumberger built cable head." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.8 hours. Operational details: Schlumberger tested primary BHA. Meanwhile, Leak tested BOP on stump to 20/345 bar for 5/10 min. Function tested BOP rams." "On 2016-04-15, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Production department started to close in well for handover." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Altus worked on lubricator and riser section. Meanwhile, Schlumberger tested B/U equipment." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to lifting BOP to moonpool area." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Lifted BOP down to moonpool area. Spooled out hoses for BOP, HMV and DHSV to moonpool." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Attempted to feed cable head (3,125'') through lubricator. Unable to due to small ID of X-over (3'') in lubricator." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Schlumberger disconnected bottom of cable head and fed cable through lubricator." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Connected GIH to lubricator section using tugger and catwalk. Spooled out and connected hoses to GIH. Meanwhile, Schlumberger re-connected cable head and began signal test to equipment." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.0 hours. Operational details: Waited while production department tested well barriers prior to handover." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Performed handover meeting between production and Intervention. Verified valve status on XMT with production representant." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Held toolbox talk prior to lifting riser and lubricator section" "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.1 hours. Operational details: Lifted and replaced permanent hatch with WL hatch." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Removed XMT top cap on well." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Lifted and connected lower riser to XMT." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Installed BOP on lower riser. Connected hoses to BOP and function tested same. Verified open / close time." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Rigged up KWV manifold and bleed-off hoses on wellhead." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Lifted middle riser section and landed on top of BOP." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to lifting lubricator to middle riser." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Lifted lubricator and GIH to middle riser. Installed Schlumberger dummy BHA in lubricator and stabbed onto middle riser." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Connected hoses for operating HMV and DHSV." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Filled lubricator with MEG from production department. Leak tested rig-up to 20/345 bar for 5/10 min." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: Purged lubricator with N2." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Verified no liquid in rig-up prior to installing perforation BHA in well. Broke lubricator and L/D Schlumberger dummy BHA." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.4 hours. Operational details: Held toolbox talk prior to installing perforation BHA in well." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.8 hours. Operational details: M/U BHA for perforation run #1 (3 3/8'' PJN guns w/ 3 1/8'' Tufftrac). Leak tested QTS to 20/345 bar 5/10 min. Dumped 40 l Starlube in lubricator." "On 2016-04-16, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Opened HMV and pressurized DHSV control line." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.3 hours. Operational details: Standby while production department used another well to equalize and open DHSV." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Opened DHSV and SV. WHP = 69 bar." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 600m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: RIH w/ run #1 (Perforation guns w/ Tractor), 3,375' OD guns by gravity from surface to 600 m." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 600m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Schlumberger performed communication check with toolstring. Meanwhile, Held well contol exercise with WL crew. Scenario: Leakage in QTS with BHA at 1500 mMD." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2810m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Continue to RIH with BHA #1 from 600 mMD to HUD at 2810 mMD taking PUW every 500m. Depth (m) PUW (lbs) Sim PUW (lbs) HW (lbs) 1000 2810 2511 2360 1500 3600 3258 3200 2000 4300 4279 3840 2500 5400 5482 4919 Actual friction factor: 0.289." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3550m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Activated tractor and continued to RIH with from 2810 mMD to 3550 mMD . Average running speed w/ Tractor: 9 m/min. Depth (mMD) PUW (lbs) Sim PUW (lbs) 3050 5450 5950 3300 5600 6270" "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3740m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Contined to RIH with tractor activated to 3642 mMD. Tractor seemed to struggle. Shut down tractor, picked up full weight and slacked off 10m. Started tractor again and RIH to 3740 mMD." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3740m. The activity was categorized as 'workover -- perforate' and lasted for 0.7 hours. Operational details: Performed orientation pass #1. Some stick and slip observed. Increased tractor arm force." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3900m. The activity was categorized as 'workover -- perforate' and lasted for 1.3 hours. Operational details: Continued to RIH with tractor activated to 3900mMD. Performed orientation pass #2 and stopped tractor." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3600m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Performed correlation logging from 3900 mMD to 3600 mMD." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3710m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Activated tractor and RIH to 3710 mMD. Tractor stalled out." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3600m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Switched to logging mode. Performed correlation pass from 3710 mMD to 3600 mMD." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3710m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Activated tractor and RIH to 3710 mMD. Tractor stalled out at same depth as previously." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3684m. The activity was categorized as 'workover -- perforate' and lasted for 0.3 hours. Operational details: Switched to logging mode and performed correlation pass. Positioned Gun 1 with bottom shots at 3684 mMD." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3684m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Perforated interval 3675 - 3684 mMD and lost 250 lbs on tension. WHP before/ after: 79,0 / 79,9 bar. A-annulus before / after: 12,4 / 12,1 bar." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3438m. The activity was categorized as 'workover -- perforate' and lasted for 0.4 hours. Operational details: Performed correlation pass for gun #2 while pulling out to 3438 mMD." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3562m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Activated tractor and RIH to 3562 mMD while performing correlation pass for gun #2." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3481m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Switched to logging mode and performed correlation pass. Positioned Gun 2 with bottom shots at 3481 mMD." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3481m. The activity was categorized as 'workover -- perforate' and lasted for 0.1 hours. Operational details: Perforated interval 3475 - 3481 mMD and lost 400 lbs on tension. WHP before/ after: 81,2 / 81,7 bar. A-annulus before / after: 12,0 / 12,0 bar." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3300m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: POOH to 3300 mMD while correlating depth." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 2.4 hours. Operational details: POOH from 3300 m to surface. WHP 84 bar." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 1.2 hours. Operational details: Closed and inflow tested SV. Closed HMV. Valve needed to be greased before test." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.3 hours. Operational details: Waited while production department greased HMV." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.6 hours. Operational details: Closed and inflow tested HMV. Purged lubricator with N2." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Held toolbox meeting prior to L/D BHA with explosives." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Broke lubricator and L/D BHA #1 (Perforation guns w/ tractor). Confirmed all shots fired." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: M/U dummy BHA for testing lubricator. Installed and stabbed lubricator. Attempted to Leak tested QTS. Found leakage in a O-ring." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.3 hours. Operational details: Changed damaged O-Ring in lubricator and leak tested same to 20/345 bar for 5/10 min." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 2.9 hours. Operational details: Closed DHSV and opened HMV. Bled down pressure in tubing to 10 bar." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 0.6 hours. Operational details: Inflow tested DHSV with 74 bar dP. Pressure increased 0,1 bar/30min." "On 2016-04-17, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Bled off pressure above DHSV before disconnecting lubricator." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Continued to bleed off tubing pressure to 0 bar. Slow progress due to unable to use PWV for bleed off." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Closed HMV. Broke lubricator and L/D dummy BHA." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: L/D lubricator and GIH on catwalk using rig crane and top drive." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Connected lifting sub to middle riser section." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Disconnected lower riser from XMT. Lifted entire riser section and BOP from XMT up to moonpool area." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Installed top cap on XMT." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Tested KWV cap and top cap to 20/345 bar for 5/10 min." "On 2016-04-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.1 hours. Operational details: Replaced WL hatch with permanent hatch. Handed well back to production. ----------------- End of Operation ---------------------" "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.8 hours. Operational details: Waited for supply vessel to arrive with straddle equipment. Meanwhile, skidded rig to F-11." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Vessel arrived rig with equipment." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Checked and verified the received straddle equipment OK." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.2 hours. Operational details: Waited while production department prepared well for handover. Meanwhile, cleaned and tidy rig floor and pipe deck." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Received well from production department." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Replaced permanent hatch with WL hatch" "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Inflow tested SV and TKV on XMT. Leak tested KWV to 20/345 bar for 5/10 min." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Hooked up chiksan manifold on KW and leak tested same to 20/345 bar for 5/10 min." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Removed top cap on XMT." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.1 hours. Operational details: Lifted riser section and BOP from moonpool area and landed on XMT." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Connected hoses for test pump and local control of DHSV and HMV on XMT." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to lifting lubricator and GIH." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Lifted lubricator and GIH from catwalk and hung off same above riser section on drill floor." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.4 hours. Operational details: M/U BHA for run #2 (Straddle w/ tractor) in Lubricator. Added 80 L starlube in riser before stabbing lubricator. Filled lubricator with MEG. Attempted to leak test rig-up to 20/345 bar for 5/10 min. Dicovered leakage in GIH due to error in Grease pump." "On 2016-04-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Waited while Altus and Maersk mechanic fixed grease pump." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Waited for Altus and Maersk mechanic to fix grease pump. Achieved good test of 345 bar on lubricator, but pump still not working as it should. Grease pump stroke increased rapidly due to pump not able to deliver enough grease pressure." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Attempted to open HMV and equalizing manifold to pressure up lubricator with N2 and displace Starlube and MEG into well. Unable to open HMV due to error in HMV pump." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Waited while Altus fixed HMV pump. Most likely caused by air in pump system." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Opened HMV and injected N2 in lubricator and bullheaded MEG/Starlube mix into well. Meanwhile, Grease pump started to work properly again." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Closed HMV and bled off pressure in lubricator." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Broke lubricator and added 80 L Starlube in riser." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Stabbed lubricator and filled rig-up with MEG. Attempted to leak test rig-up, but grease pump was unable to deliver grease pressure." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: Altus worked on grease pump issue with Maersk mechanic and electrician." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Grease pump OK. Waited for approval from onshore organisation if OK to RIH." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Leak tested lubricator to 20/345 bar for 5/10 min. Opened HMV" "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Equalized and opened DHSV. WHP = 62 bar. Observed leakage in O-ring on X-over between XMT and lower riser." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.9 hours. Operational details: Closed DHSV and bled down pressure in tubing to 3 bar." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.9 hours. Operational details: Inflow tested DHSV to 59 bar dP for 30 min." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.1 hours. Operational details: Bled off remaining pressure in tubing to 0 bar" "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.9 hours. Operational details: Closed HMV and purged lubricator with N2." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.7 hours. Operational details: Broke lubricator and L/D BHA #2 (Straddle w/ Tractor) on drill floor." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.7 hours. Operational details: Disconnected lower riser from X-over and liftet Riser section and BOP using top drive with double securing. Changed O-ring on X-over and stabbed riser back onto X-over." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Disconnected XMT from X-over and liftet Riser section and BOP using top drive with double securing. Changed O-ring on X-over and stabbed riser back onto XMT. One of the O-rings had some small marks." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.3 hours. Operational details: Closed shear ram on BOP and leak tested between SV and BOP to 200 bar for 10 min." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Lifted lubricator and GIH and hung it off above riser section using rig crane and top drive." "On 2016-04-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: M/U BHA for run #2 (Straddle w/ tractor)." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Stabbed on lubricator and leak tested rig-up to 20/345 bar for 5/10 min using 100% MEG." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.9 hours. Operational details: Opened HMV. Equalized and opened DHSV. WHP 59 bar." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2830m. The activity was categorized as 'workover -- wire line' and lasted for 2.6 hours. Operational details: RIH w/ run #2 (563-700 Straddle-Resolve-TuffTRAC; max OD 5.63' straddle) from surface to HUD at 2830 m. Performed PU every 500 m. Depth (m) PUW (lbs) 500 3000 1000 3650 1500 4650 2000 5250 2500 6550" "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3580m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Activated tractor and RIH with tractor from 2830 m to 3580 m. Average running speed 9 m/min. WHP 63 bar." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3735m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Continued RIH with tractor activated from 3580 m to 3735 m. Average running speed 8 m/min." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3745m. The activity was categorized as 'workover -- wire line' and lasted for 5.4 hours. Operational details: Performed 8 correlation passes in interval 3730 - 3640 mMD. Experienced severe stick-slip and difficulties getting on depth with correlation log." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3786m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Made 2 attempt to position BHA at setting depth by logging up from 3720 mMD. Slightly off-depth from correlation log, unable to position straddle within desired uncertainty margin. Positioned BHA on third pass by logging up from 3720 mMD to 3766.8 mMD." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3766m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Set straddle across interval 3674.4 - 3685.0 mMD. Lost 2000 lbs immediately. Tagged straddle with tractor to verify set. WHP 67 bar." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.4 hours. Operational details: POOH from 3765 mMD to surface. Average pulling speed 30 m/min. WHP 69 bar." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: Closed and inflow tested SV and HMV. Purge riser with N2." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Performed tool-box talk on drillfloor prior to L/D BHA." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Broke lubricator. L/D BHA on deck." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Checked cable head and tractor for next run." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Performed tool-box talk on drillfloor prior to M/U BHA." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.7 hours. Operational details: M/U BHA for run #3 (563-700 Straddle-Resolve-TuffTRAC)." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Stabbed on lubricator and tested QTS to 20/345 bar for 5/10 min." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Equalized and opened HMV and SV. HW 2280 lbs. WHP 71 bar." "On 2016-04-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2050m. The activity was categorized as 'workover -- wire line' and lasted for 1.6 hours. Operational details: RIH w/ run #2 (563-700 Straddle-Resolve-TuffTRAC; max OD 5.63' straddle) from surface to 2050 mMD. Performed PU every 500 m." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2830m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Continued RIH from 2050 mMD to HUD at 2830 mMD. Performed PU every 500 m. Depth (m) PUW (lbs) 500 3000 1000 3530 1500 4500 2000 5200 2500 6200" "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3490m. The activity was categorized as 'workover -- wire line' and lasted for 1.6 hours. Operational details: RIH with tractor activated from 2830 m to 3490 mMD. Average running speed 9 m/min." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3515m. The activity was categorized as 'workover -- wire line' and lasted for 2.6 hours. Operational details: Correlated multiple times across interval 3525 - 3470 mMD. Experience stick-slip and high tension (pulled maximum 9500 lbs), which affected logging quality." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3486m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Positioned straddle with top element at 3474.5 mMD. Verified depth with Petec and picked up 1.5 m to 3473 mMD to have straddle elements symmetrical over perforations." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3484m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Set straddle across interval 3473.0 - 3483.5 mMD. Lost appr. 3400 lbs on surface tension, head tension dropped 1000 lbs. Completed setting sequence and tagged straddle with tractor to verify set. WHP 77 bar." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.1 hours. Operational details: POOH from 3484mMD to surface. Average pulling speed 30 m/min." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: Closed and inflow tested HMV and SV. WHP 80 bar." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.0 hours. Operational details: Closed DHSV and bled of pressure above through PWV." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.8 hours. Operational details: Inflow tested DHSV to 0.01 bar / 30 min ." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Closed HMV and purged lubricator through XT-cross with N2." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Performed tool-box talk prior to L/D BHA on drillfloor." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.6 hours. Operational details: Broke lubricator. L/D BHA on drillfloor." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: L/D upper lubricator section and GIH to catwalk." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.1 hours. Operational details: Performed tool-box talk prior to lifting riser of well." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.9 hours. Operational details: Disconnected and lifted lower lubricator section above WL BOP to drillfloor. Lifted WL BOP from hatchdeck to PCE container. Lifted riser to cantilever deck." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.6 hours. Operational details: Installed top cap and KW cap. Rewound all BOP and PCE hoses. Installed permanent hatch." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Leak tested top cap and KW cap to 20/345 bar for 5/10 min. Meanwhile: Split lubricator on drillfloor." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Checked valve status with production operator and cleaned wellhead area. Prepared handover documention and handed well back to production dep." "On 2016-04-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.2 hours. Operational details: Packed equipment and prepared for backload." "On 2016-04-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 11.0 hours. Operational details: Packed equipment and prepared for backload. Cleaned drillfloor and cantilever." "On 2016-04-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 6.0 hours. Operational details: Performed are inspection with barge engineer. Cleaned and tidied offices and workspace. Demobilized all personell. *** End of operation ***" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed prejob meeting to skid cantilever" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Skidded cantilever onto F-11 slot, 3m to starboard" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Performed after skid jobs and cleared in moon pool area" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.0 hours. Operational details: Removed production flow line from F11B. Meanwhile L/D HPDR to cantilever, R/D diverter chains and installed elevators, spotted WL equipment on rig floor, prepared for R/U manifolds and hoses to XT" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued with preparations and R/U WL (started to R/U and check chicksan manifolds) . Meanwhile pressure tested blind flange on production wing valve" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Removed the fox hole and started to lower the wire line BOP into moon pool, continued with R/U chicksan manifolds on X-mas tree." "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: R/U top hatches in the moon pool. Meanwhile continued with lowering the WL BOP and positioning in moon pool. Lowered hoses down to WL BOP" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to remove XT cap and install lower riser and WL BOP" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Removed XT cap and installed lower riser" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to install WL BOP" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Lifted and installed WL BOP, installed hoses" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Pressure tested bleed off manifold. 20/345bar 5/10 min. Meanwhile P/U WL riser, performed housekeeping on rig floor, performed maintenance on gas trap in shaker" "On 2016-09-18, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Attempted to pressure test lower riser and WL BOP. Observed leak in the connection between lower riser and XT. Drained riser and lifted lower riser and WL BOP from XT. Secured work place. Inspected connection. Observed scratches on the internal sealing face on the XT side" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Evaluated situation. Located replacement X-over on F-04 well. Meanwhile opened BOP on stump and serviced drilling equipment" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Waited for production to prepare paperwork, isolate F-4 and bleed off pressure below tree cap. Meanwhile removed damaged X-over from F-11B XT. Built lubricator on rig floor" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Attempted to disconnect tree cap from X-over on F-4. No-go. Meanwhile opened and inspected BOP for cement" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed X-over from the XT and moved same to welders shop to attempt to release tree cap from X-over" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Release tree can from the X-over in the welders shop with help of heating" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Installed X-over on XT on F-11B well" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Installed lower riser and WL BOP on XT" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Attempted to pressure test of bleed off manifold and connection on WL lower riser to XT, 20/345bar 5/10 min. Observed leak on bleed off manifold" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshoot leak on bleed off manifold" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed pressure test of bleed off manifold and connection on WL lower riser to XT, 20/345bar 5/10 min" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to install riser and lubricator" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed cover under WL BOP. Installed riser" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed handling equipment. Installed WL lift equipment" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Lifted lubricator, M/U setting tool. Moved safety pin in sheave under elevator" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed lubricator, M/U plug BHA" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Filled riser and lubricator with 50/50 MEG. Pressure tested WL rig up to 20/345 bar 5/10 min using cement pump" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to bullhead well to sea water" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Closed SV, opened HMV. Pressured up DHSV control line to 520bar. Confirmed line up. Pumped 3m3 of 50/50 MEG w/ cement unit." "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/U to rig pump. Pumped 10 m3 wash pill w/ 1200 l/min - 124 bar" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Bullheaded 249 m3 sea water w/ 1300 l/min - 120 bar. Standpipe pressure slowly decreased and stabilised at 68 bar. Stopped pumps, SIWHP 35bar. Meanwhile performed TBT to RIH w/ deepset barrier plug" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped 10m3 50/50 MEG w/ cement pump, 1300l/min - 80bar. Closed KV on XT" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2838m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.5 hours. Operational details: Equalized and opened SV. RIH w/ run #4, deep set barrier plug to 2838 m. Average running speed 35 m/min. Tool string stopped at 2838 m" "On 2016-09-19, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2700m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: POOH from to 2700 m" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3083m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.0 hours. Operational details: RIH from 2700m. Tool string stopped at 2876m. POOH and RIH several times, worked gradually down to setting depth." "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3083m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Correlated BHA across interval 3030 - 3092 m . Set plug with mid packer element at 3083 m . Lost 300 lbs of weight after setting sequence was complete. Tagged plug" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.8 hours. Operational details: POOH from 3083 m to 0 m . Average pulling speed 35 m/min" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 3.2 hours. Operational details: Pressure tested ME550-700 plug and SV to 20/265bar for 5/10min. Bled off pressure in tubing to 10bar to closed drain. Inflow tested deepset barrier plug for 30 min. Ok. Bled off remaining pressure in tubing to closed drain. Meanwhile continued to pressure test BOP." "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D BHA (run#4)" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Broke lubricator and L/D BHA (run#4). Meanwhile serviced drilling equipment and continued with testing BOP" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Built new cablehead." "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: M/U BHA, tested DECT cutter and connected cable head. Installed lubricator" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Leak tested QTS to 20/345 bar for 5/10 min. Bleed down well pressure from 32bar to 1 bar. Opened SV" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3065m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: RIH w/ cutter BHA (run #5), to 3065 m. Running speed 35 m/min." "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3048m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Correlated across interval 3004 - 3065 m . Positioned cutter at 3055 m. Performed cut, tubing in compression. Tool stalled out. Retracted anchors" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: POOH with W/L . Average pulling speed 35 m/min" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Closed SV and leak tested tree/cross to 345 bar." "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Broke off lubricator and L/D tool string" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.2 hours. Operational details: M/U tool string w/ 572-700 ME plug (run#6), installed lubricator. Pressure tested QTS to 20/345 bar for 5/10 min. Ok" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.5 hours. Operational details: L/U to pressure up tubing. Pressured up tubing to confirm cut. Pressure went up to +/- 90 bar, then dropped to 1 bar. Observed 0.5 bar increase in annulus pressure. Continued to pump slowly with cement unit down tubing. Pressure increased both in tubing and annulus which indicated communication to annulus. Stopped pumping w/ +/- 9 bar in well. Bled off tubing pressure to 3 bar and open SV ." "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: RIH w/ shallow set plug (run#6) to 256 m. Average running speed 35 m/min." "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 276m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Correlated BHA across interval 229 - 276 m . Set plug with mid packer element at 246 m. P/U weight before/after setting 884/484 lbs. Tagged plug" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: POOH from 246 m to 0 m . Average pulling speed 35 m/min. Confirmed tool string in tool catcher and closed SV .Meanwhile held TBT for pressure testing shallow plug" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Lined up and tested shallow set barrier plug to 20bar/300bar for 5/10min. Bled off pressure to closed drain. Meanwhile TBT for rigging down wireline" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Drained lubricator and riser and purged w/ N2. Meanwhile disconnected WL BOP hoses" "On 2016-09-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: L/D lubricator, tool string, R/D sheaves" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D WL riser above BOP, L/D same" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: R/D WL BOP and lower riser joint. Removed all WL equipment from rig floor and moon pool. Pulled fox hole to be able to lift WL BOP from moon pool. Lifted WL BOP from the moon pool to the pipe deck" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting to remove hatches. Meanwhile removed BX elevator and installed chains in bails" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed split hatch on F-11. Removed hatch on adjacent well. Removed beam" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to remove X-tree and AAR for WL operation" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed lifting cap w/ tugger. Meanwhile performed pressure tests of kill/choke manifolds" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and outer ring. Meanwhile performed pressure tests of kill/choke manifolds" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lowered diverter chains on TDS bails to wellhead and attached to X-tree with double securing. Took weight as per lifting plan and removed Grayloc clamp. Meanwhile performed pressure tests of kill/choke manifolds" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lifted X-tree to moon pool. Transfered load to gantry crane in moon pool. Meanwhile performed pressure tests of kill/choke manifolds" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Attached lifting arrangement from TDS to Spacer spool. Lifted same to rig floor. Meanwhile performed pressure tests of kill/choke manifolds" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed outer ring and MB. Meanwhile Landed X-tree on skid and started to make up Grayloc clamp. Meanwhile performed pressure tests of kill/choke manifolds" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to install hatches in moon pool" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued to M/U X-tree to bracket. Installed fox hole. Installed hatches in moon pool, prepared to test TDS." "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Installed communication collar on well head using tugger line from rig floor. Meanwhile P/U riser from cantilever" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lowered HP riser to well head M/U same, installed master bushing and covers in moon pool" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Built scaffolding in moon pool for BOP/NT2 connector. Meanwhile pressure tested TDS" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lifted BOP from stump and skidded same F-11" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Troubleshoot Bop lifter , sensor fault on test stump" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Landed BOP on stump and M/U NT2 connector. Installed tension cylinder. Meanwhile drifted pipe in derrick" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Removed master bushing and installed slick joint and diverter. M/U bolts on slick joint, and removed lift gear on diverter" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pressured up diverter system, meanwhile drop checked on BOP and carried out housekeeping in moon pool" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Filled the well with sea water, using Trip tank" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressure tested connection on BOP and riser to 20/300 bar for 5/10min against shallow set plug" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Lifted casing tong to rig floor. Meanwhile broke out FOSV from side entry assembly for testing offline" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U casing tong" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U casing tong" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U THRT" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U and M/U THRT. Reconfigured pups in the string for space out" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Troubleshoot issues w/ casing tong, unable to B/O connection. Removed tong tension level and grinded same" "On 2016-09-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued to P/U and M/U tubingTHRT. POOH, installed control lines and inspected THRT" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH and landed off THRT, engaged tool and confirmed w/ 2t overpull" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Applied pressure to shear pin and then rotated string 8x turns CCW into communication collar" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pump open ME shallow set barrier plug" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Dropped 2in steel ball in the well, installed swedge to Fig. 1502 connection, installed LTV and cement hose" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressure tested cement hose and LTV to 20/345bar for 5/10 min. Confirmed line up" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Checked annulus pressure at wellhead 10bar. Started to pressure up tubing w/ cement unit with constant rate. Observed pressure drop after reaching 28 bar indicating that plug opened. Stopped pumping, pressure in tubing stabilized at 13 bar. Annulus pressure at wellhead went up and stabilized to 13 bar." "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Bled off tubing pressure above DHSV to zero and monitored for buildup, no build up observed. Applied 520bar to the control line to open DHSV. Pressured up well w/ cementing unit. Observed indications of equalizing and openning of DHSV both on cement unit and on pressure gauge on control fluid pump. Stopped pumping. Bled off well to zero pressure. Annulus pressure 2 bar. No indications of gas below DHSV/in the well observed. Confirmed zero pressure below DHSV. Closed DHSV" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3055m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RD swedge, LTV and cement hose. Meanwhile held TBT for pulling tubing hanger free" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3055m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pressured upTHRT line to 2000psi and then bled down to 500 psi to release TH" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3055m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U to 166t , neutral weight, continued to P/U to 170t, TH released (5t overpull). Continued to POOH, observed +/- 20t drag, disconnected control hoses, RIH before start breaking and L/D landing string" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3034m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: L/D landing string and THRT. Meanwhile held TBT for installing power slips and control line reel" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3034m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed power slips and positioned control line reel" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3002m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH w/ 7in tubing from 3034m 3002m" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3002m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Repaired hydraulic hose for Flush mounted slips" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3002m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull tubing" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2833m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: Continued pulling tubing from 3065m to 2833m. Average pulling speed 4,5 joints/hour" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2833m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed box protector on joint 239 w/ ME plug inside. Used crane to lay it out" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2608m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Continued pulling tubing from 2833m to 2608m. Average pulling speed 7 joints/hour" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2589m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed control line from DHSV, secured same on drum. L/D DHSV using crane. Observed back flow from well. Trip tank static. Waited for backflow to decrease" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2589m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U swedge to casing. Moved control line drum from drill floor" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2589m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D casing tong. Installed clamp on pipe for control line" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2589m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed handling gear to RIH w/ 5,5in DP" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2589m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2589m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Troubleshoot and changed linear transducer on Iron roughneck. Meanwhile built pump in tee and M/U pup joints in fox hole" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2549m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Started RIH from 2589m. Adjusted clamp, M/U 1st stand" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2549m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed casing slips and installed slips for DP" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: Continued RIH with back flow to 3050m. M/U TDS on all stands. Average RIH speed 215m/hour" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Circulated SW w/ 3000 l/min - 155bar. Observed high reading of CO of 90ppm on portable gas sensors in shacker room. Returns OIW was over 100ppm, visually dirty" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Stopped pumps, lined up to take returns to MGS, circulated w/ 1000l/min - 34bar. Confirmed zero gas readings" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Opened BOP, resumed circulation w/ 3000 l/min - 155bar. Confirmed OIW content below 30ppm after total of 193m3 circulated" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped wash pill of 20m3, 3000 l/min - 150 bar" "On 2016-09-22, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/B stand, P/U single and pump in assembly" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed cementing hose, pressure tested same to 250bar for 3 min." "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for cement job" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Balanced cement plug (3050 m - 2850 m ): Mixed and pumped 9,2 m3 of 1,9 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 2900 l of drill water. Zeroed volume counters. Displaced the cement with 46 m3 (2076 strokes) of SW, 2000 l/min/ 40 bar. Pulled out of cement to 2850m at 4 min/stand. Theoretical TOC 2850 m MD." "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2850m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: Installed sponge ball. Pumped 10m3 hi-vis at 1700l/min / 65 bar. Circulated 3000 l/min/ 140 bar. Held TBT for P/U BOP wash tool" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2800m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: POOH and R/B 1x stand. Installed closed FOSV and BOP wash tool, made 10x passes in BOP and well head at 1500 LPM / 12 bar, operated rams and annular once" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2550m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: POOH from 2829m to 2550m. Average pulling speed 280m/hour" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2550m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U casing handling equipment" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2550m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed dril pipe slips, installed casing slips. Removed CL clamp" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2550m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U casing tong" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2550m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Broke off swedge. Changed handling equipment in elevator. M/U FOSV to swedge" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1944m. The activity was categorized as 'plug abandon -- other' and lasted for 6.2 hours. Operational details: POOH with 7in tubing from 2550m to 1944m. Average pulling speed 8,2 joints/hour" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1944m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D casing handling equipment" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1944m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: R/D casing handling equipment. Cleaned and cleared rig floor" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1944m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Serviced PRSs" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1944m. The activity was categorized as 'interruption -- maintain' and lasted for 3.2 hours. Operational details: Located and repaired/changed leaking hose on aft PRS" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1944m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and B/O FOSV from tubing swedge" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1978m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U spear assembly (run #11) and engaged into 7in tubing at RKB. RIH on DP from 1944m to 1978m" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 1978m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushings and install DP slips" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2810m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Continued to RIH w/ tubing on spear from 1978m to 2810m. Average running speed 832m/hour. Meanwhile carried out TBT for pressure testing rig up of pumping lines to X-mas tree for slop injection" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 2850m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: M/U TDS and washed down with 550 l/min - 15bar from 2810m, tagged TOC at 2853.4m w/ 10t. Release spear from tubing by rotating 2x turns clockwise. Top of tubing left in the well at 909m. Meanwhile prepared to test chicksan lines to X-mas tree on F-4" "On 2016-09-23, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 436m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH w/ spear BHA (run#11) on 5,5in DP from 909 m to 436 m . Avgerage tripping speed 950 m/hour" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 40m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued to POOH w/ spear BHA (run#11) on 5,5in DP from 436 m to 40 m . Avgerage tripping speed 800 m/hour" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled spear on surface. Inspected and R/B in derrick same" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed DP slips and installed master bushing" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U jetting tool and RIH to 20.6m" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Troubleshoot pump control, unable to control mud pumps from rig floor due to PLC issue. Meanwhile carried out TBT for running pump local for jetting wellhead" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Washed wellhead w/ 1500 l/min - 28 bar , 1360 strokes pumped" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH and L/D jetting tool" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U and M/U MS-T seal retrieval tool and tested same" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH to 20.1m and engaged MS-T seal retrieval tool. Pulled seal free with 110t overpull" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH from 20m and L/D MS-T seal and retrieval tool" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U and M/U 10 3/4in cutter BHA (run#13)" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 127m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: RIH w/ 10 3/4in cutter BHA (run#13) on 5,5in DP to 127 m cutting depth" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 127m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Recorded parameters: 600 l/min - 125 bar, 400 l/min - 50 bar, 300 l/min - 25 bar, up/down weights 73t/69t" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 127m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cut 10 3/4in tieback casing at 127m 400-600 l/min, 35-50 bar, 3-7 kNm" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH w/ 10 3/4in cutter BHA (run#13) on 5,5in DP, Inspected knives, ok, L/D BHA" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U spear BHA (run#14), inspected same" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ spear BHA and engaged spear in tieback casing. Pulled fish to surface" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/U casing tong" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Released spear from tieback casing fish. R/B spear in derrick" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: R/U casing handling equipment" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 107m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull and L/D 10 3/4in casing" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.2 hours. Operational details: POOH with 10 3/4in tieback casing from 107 m to 0 m" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: R/D 10 3/4in casing handling equipment" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Changed to left hand saver sub on TDS" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U left hand torque tool with jet sub below (run#15). M/U torque to 67kNm, RIH same on left hand drill pipe from surface to 140m" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS to string and washed tieback adapter area w/ 1500 l/min - 12 bar" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Engaged and released tieback adapter w/ 15 kNm" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH w/ left hand drill pipe from 140m to surface" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed left hand saver sub" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D torque tool" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U spear BHA (run#16)" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U saver sub to TDS" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 129m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ spear to 129m, engage spear to tieback adapter fish" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH slowly w/ fish on spear to surface" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released spear and L/D tieback adapter fish" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/B spear BHA in the derrick. Meanwhile started step rate testing on F-4 well w/ cement unit" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to handle perforation guns. Meanwhile changed handling gear" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 12m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: P/U and RIH with perforation guns to 12m (run#17)" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 24m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: P/U wild single, 2x X-overs and firing head, M/U same" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: RIH w/ perforation BHA to 145m bottom shot depth" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Closed UPR, opened choke. Applied 10 bar on IBOP. Opened IBOP to confirm line up. Filled string. Opened UPR, Broke off TDS and dropped 1 3/8 ball in string. M/U TDS. Closed UPR and opened choke. Fired guns with 160 l/min - 137 bar. Top shot at 142m, bottom shot at 145m. Continued to circulate w/ 160l/min - 2 bar. No gas observed in returns" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Increased pump rate to 1000l/min -12 bar. Observed only water in returns. Circulated 1x BU, gas reading close to 0ppm in fluid and no readings in air. Stoped pumps" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min through choke, stable. Meanwhile finished pumpin step rate insection test on F-4 well" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 28m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: POOH w/ perforation BHA (run#17) from 145m to 28m" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: L/D perforation BHA (run#17). All shots fired" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U 9 5/8in casing cutter BHA (run#18)" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U 9 5/8in casing cutter BHA (run#18)" "On 2016-09-24, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: RIH w/ 9 5/8in casing cutter BHA (run#18) to 805m. Average tripping speed 1070m/hour" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 885m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Continued to RIH w/ 9 5/8in casing cutter BHA (run#18) from 805m to 885,5 m" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 885m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: M/U TDS, filled string, took parameters. 300l/min - 16 bar, 600 l/min - 80 bar" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 885m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cut 9 5/8in casing at 885,5m w/ 300-400 l/min, 19-32 bar, 80rpm, 3-7 kNm. Observed good indications of cut: pressure dropped to 0 and reduction of torque. Measured gap of 90cm" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 885m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Performed flowcheck. Observed losses of 1,6m3/hour. Losses soon stopped, totally lost of 0,3m3" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 10m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: POOH w/ 9 5/8in casing cutter BHA (run#18) from 885 m to 10 m . Avg. tripping speed 580 m/hour. Meanwhile performed TBT to inject drilling slop in F-4. Started pumping preflush w/ 1000l/min - 145bar" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D 9 5/8in casing cutter BHA (run#18)" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for drops inspection of TDS" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Carried out TDS drops inspection and service. Meanwhile continued w/ drilling slop injection on F-4. Total preflush pumped of 70m3, started pumping drilling slop, Batch#1, 1000l/min - 145bar" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: P/U side entry assembly (used in last cement job) and B/O 2x pup joints" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U 12,25 milling BHA (run#19)" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.0 hours. Operational details: P/U and M/U 12,25in milling BHA (run#19). Meanwhile continued w/ drilling slop injection on F-4. Total drilling slop pumped of 93m3 (batch#1), started pumping postflush, 1000l/min - 146bar" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 135m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: RIH w/ 12,25in milling BHA (run#19) to 135 m" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Recorded parameters: 400l/min - 2bar, 1300l/min - 6bar, 2000l/min - 9bar, 80rpm - 2-5kNm, weights up/down - 22t/15t. Tagged top of 10 3/4in subsea casing hanger at 139.7m. Meanwhile finished w/ pumping postflush after batch#1 of drilling slop on F-4. Total postflush pumped of 140m3 (after batch#1), 1000l/min - 150bar. Stopped injection for 2 hours" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 6.5 hours. Operational details: Milled 10 3/4in subsea casing hanger from 140.1 to 140.4 meter. 1500-2000l/min, 11Bar, 60-120rpm, max 25 kNm, WOB 1-8t. Observed good indications of break through: reduction of torque and WOB. Meanwhile continued w/ pumping drilling slop batch#2 on F-4. Total preflush pumped of 70m3 (before batch#2), started pumping drilling slop, Batch#2, 1000l/min - 150bar" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 140m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Run down and tagged top of 10 3/4in casing stump at 142.1m. Dressed off top of stump +/- 5 cm, 80-100rpm, 4t WOB, 2-4kNm, 2000l/min - 9bar" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 100m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Pulled up above casing hanger area and circulated 2x BU @ 3000 l/min - 21bar. Observed no losses, no gas in returns. R/B 1x stand" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 100m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Performed drops inspection on TDS. Meanwhile carried out TBT for BHA handling" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: POOH and L/D milling BHA" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U Spear assy (run#20). Checked and inspected same. RIH to 145m" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 145m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS. Engaged fish. Observed 10t overpull to pull fish free" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 747m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH with casing fish on spear. Set casing fish in slips. Bottom of casing fish at 747m. Meanwhile finished w/ pumping postflush after batch#2 of drilling slop on F-4. Total drilling slop pumped for batch#2 of 250m3, postflush pumped of 140m3 (after batch#2), 1000l/min - 150bar. Stopped injection for 2 hours" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 747m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Inspected spear, found grapple cracked. Secured grapple and R/B spear BHA in derrick. Meanwhile performed TBT to R/U casing handling equipment" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 747m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: R/U casing handling equipment for 10 3/4in casing" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 747m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting/Brief to pull 10 3/4in x 9 5/8in casing" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 747m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Removed master bushing and installed power slips" "On 2016-09-25, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 334m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 4.0 hours. Operational details: POOH with 10 3/4in casing from 747 to 334m. Average pulling speed 8,5 joints/hr. Meanwhile continued w/ pumping drilling slop batch#3 on F-4. Total preflush pumped of 70m3 (before batch#3), started pumping drilling slop, Batch#3, 1000l/min - 145bar" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 256m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Continued to POOH with 10 3/4in casing from 334 to 256m. Average pulling speed 8,7 joints/hr" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 256m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to change handling gear" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 256m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Changed handling equipment for 9 5/8in casing" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 256m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.8 hours. Operational details: Attempted to break 10 3/4in x 9 5/8in X-over. Not able to set tongs on the x-over due to no handling pup and OD of x-over bigger than collar of 10 3/4in. Repositioned x-over below and set lower tong jaws (adjustable) on x-over, confirmed length above 9 5/8in collar is not too long to pick up with elevator. Broke 10 3/4in joint from x-over and L/D x-over together w/ 9 5/8in joint" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 232m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Changed BX inserts to 9 5/8in" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.8 hours. Operational details: Continued to POOH with 9 5/8in casing from 232 to 0m. Used manual slips. Average pulling speed 7,6 joints/hr, totally pulled 61 joints. Meanwhile finished w/ pumping postflush after batch#3 of drilling slop on F-4. Total drilling slop pumped for batch#3 of 250m3, postflush pumped of 140m3 (after batch#3), 1000l/min - 150bar. Stopped injection for 2 hours" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D casing tong" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.2 hours. Operational details: R/D casing tong" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to M/U combined cutter/EZSV plug BHA (run#21)" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 13m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: P/U cutting assy and broke off taper mill. M/U M/U combined cutter/EZSV plug BHA (run#21)" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 13m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing, installed drill pipe slips" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 878m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: RIH w/ combined cutter/EZSV plug BHA (run#21) from 13 m to 878 m . Average tripping speed 500 m/hr. Meanwhile continued w/ pumping drilling slop batch#4 on F-4. Total preflush pumped of 70m3 (before batch#4), 1000l/min - 145bar" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 878m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Set EZSV @ 877.5m. Released running tool w/ +/- 25t overpull, tagged plug w/ 10 ton" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 868m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Established and recorded parameters before cutting casing. 80 rpm - 1-6 kNm, 400 l/min - 42 bar, 500 l/min - 60 bar, 600 l/min - 83bar. Cut casing @ 867.5m, 80rpm, 22 kNm, 400 l/min - 42bar. Observed good indication of cut: pressure dropped to 5 bar when cut performed, pulled up 1m and pressure increased to 42bar again. Meanwhile continued w/ pumping drilling slop batch#4 on F-4, started pumping drilling slop, Batch#4, 1000l/min - 145bar" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 868m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Flow checked well. Static. Dropped drift inside stand #22" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: POOH wet w/ combined cutter/EZSV tool BHA (run#21) from 868 m to 0 m. Avg. tripping speed 580 m/hr. Used mud bucket" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed drill pipe slips, installed master bushing" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Broke off and L/D EZSV running tool and X-overs, M/U taper mill to bottom of cutter and L/D cutter asembly" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U perforation BHA (run#22). Meanwhile changed BX inserts to 4,5in" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: P/U perforation BHA (run#22)" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 146m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: RIH w/ perforation BHA (run#22) from 15 m to 145,5 m (btm shot)" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 146m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Closed UPR, opened choke. Applied 10 bar on IBOP. Opened IBOP to confirm line up. Filled string. Opened UPR, Broke off TDS and dropped 1 3/8 ball in string. M/U TDS. Closed UPR and opened choke. Fired guns with 160 l/min - 138 bar. Top shot at 142,5m, bottom shot at 145,5m. Continued to circulate w/ 160l/min - 2 bar. No gas observed in returns" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 146m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Increased pump rate to 1000l/min. Pressure went up to 25 bar and then dropped and stabilized at 4 bar. Circulated 1x BU, observed small losses, quickly stabilized, gas reading close to 0 in fluid and no readings in air. Stoped pumps" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 146m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: Flowchecked well over the choke for 15 min. Stable. Open UPR, flow checked well with BOP open, stable. Meanwhile finished w/ pumping postflush after batch#4 of drilling slop on F-4. Total drilling slop pumped for batch#4 of 220m3, postflush pumped of 140m3 (after batch#4), 1000l/min - 145bar. Stopped injection" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: POOH w/ perforation BHA (run#22) from 146 m to 15 m" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.5 hours. Operational details: L/D perforation BHA (run#22). All shots fired" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U EZSV assembly (run#23)" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 3m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: P/U EZSV assembly (run#23)" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 845m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: P/U 2x 3m pup joints and 1x 1.5m pup joint for spaceout and RIH w/ EZSV assembly to 845m. Average running speed 480m/hour" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 845m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: M/U side entry sub assembly" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: M/U TDS and recorded weights up/down 98t/91t. Washed setting area w/ L/min. Set EZSV plug at 855,3m, tagged plug w/ 10t and keep 10t weight on EZSV" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Closed UPR, confirmed line up through the choke and MGS" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Pumped 10m3 Hi-vis pill at 900l/min - 14bar, continued to displace C-annulus to sea water, staged up pumps to 1700l/min - 38bar. Max gas 2,6%, 1-2 ppm H2S in fluid. Oil base mud in returns initially and sea water towards the end. Totally sea water pumped of 1,4x BU" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Opened UPR and closed choke, flow checked the well. Stable. Meanwhile held TBT before cement job" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Connected cement hose and LT valve" "On 2016-09-26, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 20m3 wash pill ahead of cement job, 1300l/min - 13,4bar. Verified line up for cement job" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Cement plug in C-annulus (467 m - 867 m): Mixed and pumped 33 m3 of 1,95 SG cement slurry, 600 l/min. Displaced the cement with 12m3 of drill water. 1000 l/min/ 12 bar, after caught up w/ cement pressure went up to 52 bar. Stopped pumping, pressure went down to 31bar. Pulled w/ running tool out of EZSV, pressure dropped to 0 bar" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Disconnected cementing hose and L/D side entry sub. M/U pup w/ preinstalled sponge ball" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 855m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Lined up and pumped 10m3 wash pill, 2300l/min - 20bar. Circulated well to clean sea water until OIW reading below 30ppm. Originally mud in returns and clean sea water in the end. Max gas 3.2%. Totally circulated 108 m3, 2x BU" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 11m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: POOH w/ EZSV running tool from 855 m to 11 m, average pulling speed 850m/hour" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: L/D 3x 5,5in pup joints and EZSV running tool" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: WOC (from 01:20). Meanwhile isolated both PRSs and carried out 3 monthly PMS" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.0 hours. Operational details: WOC. Meanwhile started with maintenance on forward and aft PRS. Meanwhile continued w/ pumping drilling slop batch#5 on F-4. Total preflush pumped of 70m3 (before batch#5), started pumping drilling slop, Batch#5, 1000l/min - 145bar" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: WOC. Meanwhile continued to perform maintenance on forward and aft PRS" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.5 hours. Operational details: WOC. Work aloft suspended due to wind speed above 50 knots. Gusting upto 60 knots. Performed high wind checks. Meanwhile performed rig PMs and maintenance" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: WOC. Wind speed 52-59 knots. Continued rig floor maintenance and PMs. Prepared to clean mud pits. Hooked up line from F-09 to rig choke manifold to bleed off gas. Meanwhile finished w/ pumping postflush after batch#5 of drilling slop on F-4. Total drilling slop pumped for batch#5 of 170m3, postflush pumped of 140m3 (after batch#5), 1000l/min - 145bar" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: WOC. Wind speed now below 48 knots, continued to work on aft PRS. Continued to hook up line from F-09 to rig choke manifold. Started cleaning in mud pit No. 5" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: WOC. Performed maintenance on TDS. Continued to hook up line from F-09 to rig choke manifold. Continued cleaning in mud pit No. 5" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Deisolated TDS" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to change grapple on 10 3/4in spear" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Changed grapple on 10 3/4in spear BHA for the well of F-4" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: P/U MST tool and M/U to 5,5in DP, RIH to 20m" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 20m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed Master Bushings and install PS21 slips" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: RIH w/ MST tool on 5,5in DP from 20m to 808m, average running speed of 790m/hour. Meanwhile lined up and started pressure testing surface lines" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Closed UPR, performed line test to 120 bar, good test" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Closed IBOP, lined up to test the well with cement unit. Pressure tested C-annulus surface cement plug to 115bar for 10min. Good test" "On 2016-09-27, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 808m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Broke off TDS and spaced out for cement job" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 853m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: P/U and M/U side entry sub assembly, installed cement hose" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 853m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to place balanced cement plug" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 853m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 10m3 wash pill. Staged up rate to 2200l/min - 16bar" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 853m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Balanced cement plug (755 m - 855 m ): Mixed and pumped 8 m3 of 1,95 SG cement slurry, 600 l/min. Zeroed volume counters. Displaced the cement with 9m3. 1000 l/min - 12 bar. Caught up with cement, pressure increased to 25bar. Theoretical TOC 755 m MD" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 655m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pulled out of cement to 655m at 2 min/stand." "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 655m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: M/U pup w/ pre-installed sponge ball. Circulated above cement plug at 3300 l/min - 30 bar, 50 RPM. Diverted returns overboard. Total circulated 75m3 (1,7x BU)" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: POOH w/ MST tool from 655m to surface. Average tripping speed of 870 m/hour" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed PS21 and installed master bushing" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Broke off stand#1 and R/B same, L/D MST tool" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: M/U BOP jetting tool to stand#1. Jet BOP 1400l/min - 24 bar - 40 rpm. Function tested BOP. L/D BOP jetting tool and R/B DP stand" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to N/D diverter" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Drained riser, meanwhile removed BX elevators and rotator. Installed lifting chains for diverter to bails" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled master bushing and outer ring, attached lifting chains to diverter. Bled down pressure on diverter, disconnected overshot hose" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled diverter and secured same on DP set back area" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Disconnected and pull slick joint to rig floor. Meanwhile hook up bleed off line to F-09" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to release BOP tension system" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Removed BOP tension cylinders. Meanwhile continued w/ pumping drilling slop batch#6 on F-4. Total preflush pumped of 70m3 (before batch#6), started pumping drilling slop, Batch#6, 1000l/min - 140bar" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Skidded BOP from well center to test stump. Meanwhile perform maintenance on FWD PRS. Emptied skimmer tank" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Dismantled scaffolding from well center. Meanwhile performed maintenance on FWD PRS" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed master bushing and outer ring in RKB" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D high pressure riser" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Connected lifting gear and pulled HP riser, L/D same" "On 2016-09-28, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Removed split hatches on F-11 and installed solid cover. Meanwhile ventilated gas from annulus on F-09 to rig choke. Meanwhile finished w/ pumping postflush after batch#6 of drilling slop on F-4. Total drilling slop pumped for batch#6 of 123m3, postflush pumped of 140m3 (after batch#5), 1000l/min - 137bar REPORTING ON F-9A" "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding rig to F-11 B" "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Skidded cantilever to well F-11 B" "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed post-skid checks." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Removed hatch. Built scaffolding around hole opening in moonpool. Meanwhile: Installed deck hatches on well F-12." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Removed scaffolding on WH deck to access well F-11. Meanwhile: Changed elevator." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lowered and N/U NT2 connector. Installed master bushing." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U and M/U BHA and inner string." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Engaged Multibowl RT to Multibowl. Confirmed with 20 ton overpull." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Load shifted weight from tension cylinders to TDS. N/D tension cylinders and boat collision stool. Built scaffolding around hole opening." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Staged up flow rate to 2400 lpm / 80 bar. Cut riser at 134,9m. Observed loss of overpull, good indication of cut." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/D hoses and valve outlets from Multibowl. Pulled master bushing." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled Multibowl, riser and inner string to drill floor. Installed master bushing and C-plate. Laned off Multibowl onto C-plate." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS and B/O Multibowl RT. R/B same." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U false rotary and C-plate." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with inner string. R/B cutter BHA." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U Mutlibowl RT." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH with riser (Lift #1). Cleaned off marine growth on centralizer deck. Meanwhile: Performed TBT for L/O Multibowl and tensioner joint." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine" "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Attempted to cut riser. Significant wave height 0,8m Observed vibrations after cut a few millimeters into the tensioner joint. Cutter jammed several times." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew" "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Re-aligned cutter and started new cut. Cut riser, vibrations still present. Significant wave height 0,7m. R/D cutting machine." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O Multibowl and tensioner joint. Removed Multibowl RT and NT2 connector." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (Lift #2). Cleaned off marine growth on centralizer deck. Landed off riser onto elevator." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser, no further vibrations observed. Significant wave height 0,8m R/D cutting machine" "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #2). Pulled riser (Lift #3). Cleaned off marine growth on centralizer deck. Landed off riser onto elevator." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 0,7m R/D cutting machine." "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #3). Pulled riser (Lift #4). Cleaned off marine growth on centralizer deck. Landed off riser onto elevator. Riser out of splash zone at 23:30" "On 2016-10-20, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. R/D cutting machine." "On 2016-10-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #4). Pulled riser (Lift #5). Cleaned off marine growth on centralizer deck. Landed off riser onto elevator." "On 2016-10-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #5). Pulled riser (Lift #6). Cleaned off marine growth on centralizer deck. Landed off riser onto elevator." "On 2016-10-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O riser joint (Lift #6). Pulled riser (Lift #7). L/O last riser joint." "On 2016-10-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-10-21, at Well NO 15/9-F-11 B, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed hatches and hole covers in moonpool and WH deck. Removed scaffolding. *** END OF REPORT ***" "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to skidding rig from F-9 to F-1." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.2 hours. Operational details: Skidded rig port. Started to skid rig/cantilever forward." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.2 hours. Operational details: Skidded rig/cantilever forward to slot F-1. Picked up stabd of drillpipe and ran through F-1 slot. Checked allignment over slot and made adjustments accordingly. Built scaffolding around F-1 wellslot. Installed 2nd hatch in moonpool." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up 36' holeopener BHA." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 9m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Picked up 36' x 26' x 17 1/2' holeopener and hung off in RT. Removed dog collar on drill guide bushing. Made up holeopener to BHA." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 133m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Made up DC and ran in with 36' holeopener BHA to 133 m MD." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 144m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: While observing with ROV, stabbed BHA into funnel at 140 m MD. Tagged seabed at 144,3 m with 5 MT WOB." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Washed down from 144 m to 145 m with 1000 lpm." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 36' hole section from 145 m to 165 m MD with reduced drilling parameters : Flow 600-1000 lpm / Rotation 10-25 rpm / WOB 1-3 MT / Torque 3-16 kNm. ROV observed that drill guide bushing landed in funnel. Survey at 165 m MD 0,21 deg. High torque and excessive rattling in string from 160-165 m MD." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: Drilled 36' hole section from 165 m to 17 1/2 TD at 226 m MD / 36' TD at 223 m MD. Drilling parameters : Flow 4100-4400 lpm / Rotation 70-90 rpm / WOB 1-3 MT / Torque 5-7 kNm. Swept hole with 20 m3 hi-vis before connection. Performed survey every 10 m. Final survey at 226 m MD 0,18 deg." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Ciruculated hole clean by pumping 1,5 x hole volume of seawater while reaming with 10 rpm." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pumped 25 m3 hi-vis sweep followed by 60 m3 sewater at 4400 lpm. Mechanical popoff on mudpump #3 triggered unintentionally, no pressure spike observed. Discussed situation. Decided to continue operations and displace to 1,40 sg mud using only one mudpump." "On 2007-12-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Displaced hole from seawater to 1,40 sg WBM pumping with a limited rate of 2200 lpm." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued to displace well to 1,40 sg WBM with limited rate of 2200 lpm. Pumped a total of 95 m3 1,40 sg WBM." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 215m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: POOH with 36' holeopener BHA from 226 m to 215 m MD. Observed 10 MT overpull at 215 MD. Pipe free to move down. Applied 5 rpm rotation and pulled through thightspot while rotating. Stopped rotating at 213 m MD and continued pulling, no excessive drag observed." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH with 36' holeopener BHA from 213 m to 150 m MD on 5 1/2' HWDP. Topped up well with 5 m3 1,40 sg WBM pumping at 1000 lpm." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 128m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pulled 36' holeopener through template funnel to 128 m MD. Pumped 20 m3 seawater at 1800 lpm to clean string and surface lines." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Pulled and racked back BHA. Broke out and laid down 9 3/4' DC and MWD." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Laid out 36' x 26' x 17 1/2' holeopener and prepared for backload." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Transported 1 x tension cylinder from drillfloor to Centralizer deck using tugger. Performed FG-check in derrick." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to rigging up 30' conductor handling equipment." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Removed drilling bails and elevator. Installed conductor bails and elevator. Brought conductor running equipment to riigfloor." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk prior to running conductor." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed masterbsuhing and installed 30' conductor inserts in rotary." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up float shoe and hung off. Picked up conductor joint and made up to shoe. Filled shoe and checked for flowthrough - ok." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 68m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Ran 30' conductor from 20 m to 68 m MD." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 68m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held toolbox talk prior to changing handling gear. Changed from conductor bails/elevator/insert to 5 1/2' handling equipment." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Held toolbox talk prior to picking up 30 conductor housing. Made up conductor housing to conductor, applied 33000 ft lbs m/u torque. Ran in with conductor to 82 m MD. Installed C-plate in rotary and landed conductor. Removed handling CART. Filled 30' conductor with 14 m3 seawater. Meanwhile held toolbox talk for running innerstring." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Installed C-plate on top of conductor housing. Ran 7 ea 4 3/4' aluminum innerstring joints inside conductor. Installed centralizer on joint #2. Changed seals on running CART. Made up CART to innerstring. Installed inclinometer and fillup valve handle on CART. Reading on inclinomenter : pitch 0,3 / roll 0,1." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Landed CART in conductor housing and made up to same by 5 lefthand turns." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 85m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up conductor and removed C-plate in rotary. Ran conductor below rotary and installed masterbushing, hung off on slips." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 112m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up 5 1/2' DP double and RIH with conductor. Guided conductor through Centralizer deck using sling and chainhoist." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran in hole with 30' conductor on dedicated landing string to 138 m MD to put top of conductor below sealevel. Filled conductor with with 16 m3 seawater at 2000 lpm. Hookload after filling 110 MT." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Stabbed conductor into guide funnel while observing with ROV. Ran in with conductor to 221 m MD and landed 10 cm below 112,88 m mark on pipe relative to Centralizer deck. Meanwhile engaged hotstab in bank #1 on template base and shifted handle to 'on'. Hookload at TD 100 MT, no excessive drag observed in hole." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made digiquartz measurement indicating that conductor housing F-1 was 45 mm higher than reference well F-7." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Adjusted height of conductor by comming down 3 cm. Made new digiquartz measurement indicating F-1 25 mm higher than reference well F-7 - ok. Read inclinometer on CART : pitch 0,3 / roll 0,11." "On 2007-12-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Attempted to pressure up on hotstab to energize centralizing pistons in funnels - nogo - observed that hotstab was leaking / rapid pressure bleed off. Worked hotstab further in and re-attempted pressuring up. Correct indications on pump with regards to volume and steady 2000 psi pressure on pump, but no movment of pistons could be observed. Attempted to move handle which was bent and fell off. Discussed situation. Decided to go ahead with cement job. Meanwhile leaktested lineup from cement unit to lo-torque to 200 bar / 10 min - ok." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made x-y measurements on conductor relative to funnel : fwd 38 cm / aft 34 cm / stb 34 cm / port ?? cm (unreliable data due to bad access)." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated hole to seawater before cementing. Stepped pumps up to 1500 lpm. No annulus returns could be observed by ROV. Inspected template for returns elsewhere but none could be observed. No return observed after 60 m3 pumped. Hookload rose from 100 MT to 110 MT during displacement indicating lighter fluid in annulus." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Increased pump rate to 2000 lpm. Pumped another 40 m3. After 15 min pumped, observed returns from annulus. Hookload levelled out at 112 MT." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Attempted to mix and pump cement. Had severe problems transferring dry X-lite cement from bulk system to surge tank. Automatic transfer system was not working. Could not keep a steady transfer rate by manual operation. Not possible to obtain prescribed cement slurry. Pumped 12 m3 cement of varying weights at slow rate. Aborted operation." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Displaced cement to drillfloor and circulated out same by pumping 40 m3 of seawater at 2000 lpm with rigpumps. Meanwhile washed cement unit and troubleshot bulk transfer system. Rig air pressure insuffcient to operate cement bulk system." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Started cementing. Hookload before start 109 MT." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Mixed and pumped 60 m3 1,52 sg tuned light cement slurry. Pump rate 800-1100 lpm. Pump pressure 20 bar. Displaced cement with 6,5 m3 seawater to put theoretical top of cement at 217 m MD inside conductor. Hookload during cementing fell from 110 MT to 100 MT indicating annulus displaced to heavier fluid." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed lo-torque on cement strand. Broke off cement hose and flushed manifolds." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 11.5 hours. Operational details: Waited on cement to set up. Meanwhile : -Retrieved hotstab and guidewire -Continued work on aft PRS -Installed new rubber conveyor belt on HTS -Started work on tensioner cylinders on F-14 -General PM on drillfloor" "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Performed toolbox meeting prior to disconnecting CART. Slacked off 10 MT to obtain neutral at CART. Disconnected CART from conductor housing with 5 righthand turns. Lifted out CART and set slips on landing string. Broke out and laid down cementing stand. Pumped 2 ea sponge balls at 2500 lpm to clean string. Reading on inclinometer before disconnect : pitch 0,34 deg / roll 0,06 deg." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: POOH with CART tool on 5 1/2' HWDP landing string. Racked back landing string. Broke out and laid out CART for backload. Meanwhile the ROV checked elevation of conductor housing with digiquartz. F-1 was 5 mm higher than reference well F-7." "On 2007-12-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with 4 3/4' aluminium innerstring using tugger and clamps. Cleared and tidied drillfloor." "On 2007-12-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed hatches in wellhead module slot F-1 with tugger support from drillfloor. Removed/moved scaffolding barriers in wellhead module as required. Removed stairs to cantilever in preparation for skidding. Meanwhile ROV dredged to access CTS hose which was burried in mud/cuttings. ****Transferred operations to F-14****" "On 2013-07-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Held tool box talk. Skidded rig 2.1 m port." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Skidded rig 2.95 m total port and positioned well center above slot F-1." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 5.5 hours. Operational details: Changed out topdrive saver sub and leak tested wash pipe. Changed handling equipment and cleared rig floor of excess equipment. Meanwhile: Prepared 26' steerable BHA." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 36m. The activity was categorized as 'drilling -- trip' and lasted for 6.2 hours. Operational details: P/U and M/U 26' mud motor steerable BHA to 36 m. Plugged-in MWD tools. Observed communication problems between Bi-communicational pulse module and gyro sub." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Troubleshoot tool communication failure." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: P/U and M/U 26' mud motor steerable BHA to 103 m. *ROV in for close cover." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH with 26' BHA on 5 1/2' HWDP from 103 m to 130 m and removed debris cap from cuttings transport system. *ROV in for close cover." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH with 26' BHA on 5 1/2' HWDP from 130 m to 145 m inside 30' conductor." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: R/U gyro wireline sheaves and wire" "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 184m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH with 26' BHA on 5 1/2' HWDP from 145 m to 184 m." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 212m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: RIH with 26' BHA on 5 1/2' DP from 184 m to 212 m." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 212m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Recorded Up/Dn weight, 98/95 MT and established washing parameters with 2500 lpm, 3 bar, 20 rpm, 3 kNm." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Washed down from 212 m and tagged TOC at 217 m with 2 MT." "On 2013-07-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled out cement, float and rat hole from 217 m to 226 m with 3500 lpm, 85 bar, WOB 1-2 MT, 60 rpm, 3-.6 kNm." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Cleaned out rat hole and reamed same 3 times with 3500 lpm, 85 bar, 60 rpm, 0-1 kNm." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 219m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: Run wireline gyro. Orientated mud motor tool face and retrieved gyro. Meanwhile: Torque-up wash pipe connection." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 252m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Established drilling parameters. Drilled and orientated 26' hole from 226 m to 252 m with 2500-3000 lpm, 60-70 bar, WOB 10-14 MT, Average ROP 10 m/hr. *Drilled new formation at 02:50 hrs." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 238m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: R/U and run wireline gyro. Recorded single shot gyro and R/D wireline." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 292m. The activity was categorized as 'drilling -- drill' and lasted for 8.8 hours. Operational details: Drilled and orientated 26' hole from 252 m to 292 m with 4500 lpm, 140 bar, 90 rpm 8-15 kNm, WOB 5-10 MT, Average ROP 5 m/hr, Slid/rotation ratio 35/65 %" "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 292m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Inspected top drive. Observed oil leak on oil cooler. Recorded on bottom survey." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 211m. The activity was categorized as 'interruption -- repair' and lasted for 2.8 hours. Operational details: POOH with 26' BHA on 5 1/2' DP from 292 m to 211 m inside 30' conductor. Isolated drill floor equipment and changed out leaking fitting on top drive. Meanwhile Completed testing of X-mass tree on F-11." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 280m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with 26' BHA on 5 1/2' DP from 211 m to 280 m. Recorded 5 MT down weight." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 292m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Worked string pass restriction from 280 m to 292 m with 3000 lpm, 65 bar, 30 rpm, 7 -14 kNm." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 323m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled 26' hole from 292 m to 323 m with 4500 lpm, 145 bar, 90 rpm, 4-8 kNm, WOB 3 MT, Average ROP 11 m/hr." "On 2013-07-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 333m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Orientated tool face. Drilled and orientated 26' hole from 323 m to 333 m with 4500 lpm, 135 bar, WOB 1-7 MT, Average ROP 10 m/hr." "On 2013-07-24, at Well NO 15/9-F-1, a drilling event occurred at a depth of 413m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled and orientated 26' hole from 333 m to 413m with 3500 lpm, 95 bar, 60 rpm, 7-9 kNm, WOB 3-8 MT, ROP drilling : 30 m/hr. Pumped 10m3 hi-visc sweep every 15m. Recorded survey on every single." "On 2013-07-24, at Well NO 15/9-F-1, a drilling event occurred at a depth of 413m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Made several attempts to take survey with MWD gyro - no go." "On 2013-07-24, at Well NO 15/9-F-1, a drilling event occurred at a depth of 413m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to rig up to run wireline gyro." "On 2013-07-24, at Well NO 15/9-F-1, a drilling event occurred at a depth of 413m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: Rigged up to run wireline gyro and performed survey." "On 2013-07-24, at Well NO 15/9-F-1, a drilling event occurred at a depth of 441m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled and orientated 26' hole from 413 m to 441m with 3700lpm, 115bar, 0-60 rpm, 2-6 kNm, WOB 5-10 MT, ROP drilling : 50 m/hr. Pumped 10m3 hi-visc sweep every 15m. Recorded survey on every stand with wireline gyro." "On 2013-07-24, at Well NO 15/9-F-1, a drilling event occurred at a depth of 441m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Attempted to perform MWD gyro survey 2 times - no go." "On 2013-07-24, at Well NO 15/9-F-1, a drilling event occurred at a depth of 615m. The activity was categorized as 'drilling -- drill' and lasted for 11.2 hours. Operational details: Drilled and orientated 26' hole from 441m to 615m with 3700-4000lpm, 117-132bar, 0-60 rpm, 6-14 kNm, WOB 5-8 MT, ROP drilling: 35 m/hr. ROP sliding: 25 m/hr Pumped 10m3 hi-visc sweep every 15m. Recorded survey on every stand with wireline gyro." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 655m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled and orientated 26' hole from 615m to 655m with 3700lpm, 116-118bar, 0-60 rpm, 4-14 kNm, WOB 4-8 MT. ROP drilling: 30 m/hr. ROP sliding: 20 m/hr. Pumped 10m3 hi-visc sweep every 15m." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 655m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Ran in hole with wireline gyro and performed survey. Pulled out of hole with wireline gyro." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 696m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and orientated 26' hole from 655m to 696m with 3700lpm, 118-120 bar, 0-60 rpm, 5-11 kNm, WOB 4-7 MT. ROP drilling: 50 m/hr. ROP sliding: 30 m/hr. Pumped 10m3 hi-visc sweep every 15m." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 696m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Ran in hole with wireline gyro and performed survey. Pulled out of hole with wireline gyro." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 736m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled and orientated 26' hole from 696m to 736m with 3700lpm, 118-120 bar, 60 rpm, 4-15 kNm, WOB 6-10 MT. ROP drilling: 30 m/hr. ROP sliding: 20 m/hr. Pumped 10m3 hi-visc sweep every 15m." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 736m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Ran in hole with wireline gyro and performed survey. Pulled out of hole with wireline gyro." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 776m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and orientated 26' hole from 736m to 776m with 4000 lpm, 136-137 bar, 0-60 rpm, 8-20 kNm, WOB 9-13 MT. ROP drilling: 50 m/hr. Pumped 10m3 hi-visc sweep every 15m." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 776m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Ran in hole with wireline gyro and performed survey. Pulled out of hole with wireline gyro." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 776m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: Made up top drive and performed MWD surveys at 776m MD, 757m MD and 739m MD. Performed MWD check surveys." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 817m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled and orientated 26' hole from 776m to 817m with 4000 lpm, 132-133 bar, 60 rpm, 10-14 kNm, WOB 8-11 MT. ROP drilling: 40 m/hr. Pumped 10m3 hi-visc sweep every 15m." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 817m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Rigged down wireline equipment and laid down to deck." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 897m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled and orientated 26' hole from 817m to 880m with 4000 lpm, 133-137 bar, 0-60 rpm, 11-17 kNm, WOB 10-14 MT. ROP drilling: 40 m/hr. Pumped 10m3 hi-visc sweep every 15m. Performed MWD surveys on every stand." "On 2013-07-25, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1034m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled and orientated 26' hole from 880m to 1034m with 4000-4500 lpm, 133-170 bar, 0 rpm, 0 kNm, WOB 4-6 MT. ROP sliding: 60-90 m/hr. Pumped 10m3 hi-visc bentonite sweep every 15m. Performed MWD surveys on every stand." "On 2013-07-26, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1065m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and orientated 26' hole from 1034m to 1065m with 4000 lpm, 133-135 bar, 0 rpm, 0 kNm, WOB 4-6 MT. ROP sliding: 40 m/hr. Pumped 10m3 hi-visc bentonite sweep every 15m. Performed MWD surveys on every stand." "On 2013-07-26, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1130m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Drilled and orientated 26' hole from 1065m to 1140m with 4000-4500 lpm, 133-176 bar, 0-60 rpm, 9-15 kNm, WOB 10-16 MT. ROP drilling: 20 m/hr ROP sliding: 15 m/hr. Pumped 10m3 hi-visc sweep every 15m. Performed MWD surveys on every stand." "On 2013-07-26, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1220m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 26' hole from 1140m to 1220m with 4500 lpm, 175-176 bar, 60 rpm, 7-12 kNm, WOB 6-12 MT. ROP drilling: 25 m/hr Pumped 10m3 hi-visc sweep every 15m. Performed MWD surveys on every stand. Reamed full stand in upper Hordaland Group." "On 2013-07-26, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1260m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Slided and oriented 26' hole from 1220m to 1260m with 3600-4000 lpm, 126-143 bar, 0 rpm, 0 kNm, WOB 10-16 MT. ROP drilling: 15 m/hr Pumped 10m3 hi-visc sweep every 15m. Performed MWD surveys on every stand. Reamed full stand in upper Hordaland Group." "On 2013-07-26, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 26' hole from 1260m to 1355m with 4500 lpm, 178-179 bar, 60 rpm, 9-15 kNm, WOB 7-12 MT. ROP drilling: 40-60 m/hr Pumped 10m3 hi-visc sweep every 15m. Performed MWD surveys on every stand. Reamed full stand in upper Hordaland Group." "On 2013-07-26, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.5 hours. Operational details: Circulated hole clean by pumping 2 x bottoms up with 4500 lpm and 158 bar." "On 2013-07-26, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Displaced hole with 1.35 sg KCl water based mud with 4500 lpm and 120-176 bar." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1245m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 1355m MD to 1245m MD. At 1245m MD took 10MT overpull. Attempted to get past restriction several times up to 30MT - no go. Attempted to pass restriction with 10 rpm - no go - string torqued up at 30 kNm." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1222m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Lubricated out of hole with 26' bottom hole assembly at 500 lpm seawater and 10 rpm from 1245m MD to 1222m MD. Pumped a total of one string volume. Attempted to pull string without circulation with up to 25MT - no go." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1182m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Lubricated out of hole with 26' bottom hole assembly at 1000 lpm and 10 rpm from 1222m MD to 1182m MD." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 543m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 1182m MD to 543m MD. At 543m MD, observed 30MT overpull." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 506m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Lubricated out of hole with 26' bottom hole assembly from 543m MD to 506m MD with 1500 lpm and 30 rpm." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 347m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 506m MD to 347m MD. Observed tight spots at 505m MD, 488m MD, 479m MD and 440m MD with maximum 30MT overpull." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 347m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned PS21 slips due to excessive clay on pipe body." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 347m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to perform wiper trip to TD." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 347m MD to 221m MD. Observed tight spots at 284m MD and 272m MD with maximum 20MT overpull." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- ream' and lasted for 0.2 hours. Operational details: Established circulation at 4500 lpm and 128 bar to clean bottom hole assembly for clay." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- ream' and lasted for 8.2 hours. Operational details: Ran in hole with 26' bottom hole assembly from 221m MD to 1355m MD. Washed and reamed areas from 381m - 390m, 1317m - 1328m and 1328m - 1355m with 3000 lpm, 72-80 bar and 40 rpm." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pumped 20m3 hi-visc, 30m3 seawater, 30m3 hi-visc and 100m3 seawater at 3000 lpm, 72 bar and 40 rpm." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Displaced hole to 1.35 sg KCl water based mud at 4600 lpm and 177 bar." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1287m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 1355m MD to 1334m MD. At 1334m MD observed 20MT overpull. Attempted to pass restriction several times with up to 45MT overpull - no go. Lubricated past restriction with 300 lpm from 1334m MD to 1287m MD with 30MT overpull." "On 2013-07-27, at Well NO 15/9-F-1, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 1287m MD to 350m MD. Observed tight spots at 1040m MD, 635m MD and 556m MD with maximum 10MT overpull. Meanwhile: While pulling out of hole, ROV jetted drillstring at seabed due to excessive clay on pipe body with good success." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pulled out of hole with 26' bottom hole assembly from 250m MD to 221m MD. Meanwhile: Commenced shutting down producing wells F-11, F-12 and F-14." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Topped up hole with 1.35 sg KCl water based mud. Serviced top drive and drill floor equipment. Greased dolly." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 51m. The activity was categorized as 'drilling -- trip' and lasted for 3.8 hours. Operational details: Pulled out of hole and laid down 26' bottom hole assembly from 221m MD to 51m MD." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 51m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Downloaded MWD." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Pulled out of hole and laid down 26' bottom hole assembly from 51m MD to deck." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Removed CTS from 30' conductor. Installed cap on top of conductor. Connected control and cement hoses. Installed storm line sheave. Racked back cement head in derrick." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Performed prejob meeting prior to rig up to run 20' casing." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 5.2 hours. Operational details: Rigged up to run casing. Installed casing tong, removed drilling bails and elevator. Made up lafleur. Installed casing bails and elevator." "On 2013-07-28, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: Waited on weather. Cranes down due to wind speed above 40 knots. Meanwhile: Function tested rig up, slips, elevator, tongs and HTS." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: Waited on weather. Cranes down due to wind speed above 40 knots." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up shoe joint from deck and set it in slips. Installed dog collar and verified float by hosing water through it." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 9.5 hours. Operational details: Troubleshoot elevator, not able to function open position. Laid out 20' shoe joint and weatherford elevator. Rigged up BX3 elevators and rotator." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to running 20' casing." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and backup shoe joint and landing joint from deck and made up with tread lock. Verified floats by hosing water through it." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Ran in hole with 20' casing from 25m MD to 138m MD." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Attempted to stab 20' casing into 30' conductor - no go. Rigged up chain hoists and guided 20' casing into 30' conductor." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 176m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed DROPS check of top drive." "On 2013-07-29, at Well NO 15/9-F-1, a drilling event occurred at a depth of 515m. The activity was categorized as 'drilling -- casing' and lasted for 6.2 hours. Operational details: Ran 20' casing from 176m MD to 515 m. Average running speed: 4.5 joints / hr. Observed 20MT weight at 504-510m MD" "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- casing' and lasted for 8.8 hours. Operational details: Ran 20' casing from 515m MD to 1198m MD. Average running speed: 6.5 joints / hr." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up and make up 18 3/4' wellhead." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Laid out weatherford circulating tool. Changed out to 5 1/2' handling equipment." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1213m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up and made up 18 3/4' wellhead to 20' casing. Prepared wellhead for running in hole." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1213m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Changed out PS30 slips and installed master bushings." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1213m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to rigging down weatherford casing tong." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1213m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Rigged down weatherford casing equipment and laid out to deck." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1335m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Ran in hole with 20' casing on 5 1/2' heavy weight drill pipe from 1213m MD to 1312m MD. At 1312m MD, observed 15MT weight. Established circulation in stages to 1500 lpm and 39 bar. Washed down with 20' casing on 5 1/2' heavy weight drill pipe from 1312m MD to 1335m MD." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1335m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up cement stand to 5 1/2' heavy weight drill pipe." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Washed in hole with 20' casing at 1500 lpm and 40 bar from 1335m MD to 1348m MD. Landed and locked wellhead. Confirmed wellhead latched by applying 20MT overpull." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Circulated 2 x bottoms up with 2300 lpm and 18-27 bar. Meanwhile: Performed prejob meeting prior to performing cement job." "On 2013-07-30, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Closed IBOP and applied 30 bar above. Opened lo-torque and dropped ball. Mixed and pumped 304m3 1.56sg lead slurry and 30m3 1.92sg tail slurry." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Continued mixing and pumping 304m3 1.56sg lead slurry and 30m3 1.92sg tail slurry. Meanwhile: Made ready equipment for running high pressure drilling riser. Tranfered claxton tool to drill floor and attached sub. Performed general maintanence and house keeping." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Dropped top dart and pumped 1200 liters behind with cement unit. Observed top wiper plug sheared out with 145 bar. Closed lo-torque and opened IBOP. Displaced cement with 9669 strokes (theoretical volume + 1/2' shoetrack. Used 97% pump efficiency). No bump observed. Final circulating pressure observed was 60 bar at 1400 lpm." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up down to cement unit. Bled back 540 liters to cement unit. Observed for backflow for 15 minutes - no backflow observed." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Isolated drilling equipment for manriding. Removed control lines and cement hose from cement head." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released overpull on running tool to neutral weight. Released 18 3/4' wellhead running tool by to turning 5 times clockwise. Pulled same above wellhead." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Racked back cement stand in derrick. Dropped 2 x wash balls into string. Made up new stand." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 130m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Jetted area around wellhead with 3000 lpm and 8 bar." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Pulled out of hole with 18 3/4' wellhead running tool on 5 1/2' heavy welght drill pipe from 130m MD. Laid out same to cantilever." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Laid out claxton running tool to cantilever." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Broke out cement stand and laid out same to cantilever. Made up single 5 1/2' heavy weight drillpipe and racked back stand." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to start rig up to run high pressure drilling riser." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up and made up riser spider. Installed in rotary and function tested same." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.2 hours. Operational details: Rigged up to run high pressure drilling riser. Ran wellhead guide funnel and installed same in wellhead. Installed sheave and holdback lines. Installed tension ring on F-1 and teflon centralizers. Serviced top drive and installed VX gasket on wellhead." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to start picking up and run heavy weight drilling riser." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up TBC / stress joint and ran through rotary, landed same in spider." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up lower riser pup joint. Prepared seal faces on joint connection and made up same." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Function tested TBC in moonpool - ok. Verified valve positions." "On 2013-07-31, at Well NO 15/9-F-1, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up and made up intermediate riser joint #4." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 50m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Ran in hole with high pressure drilling riser from 35m to 50m." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 64m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Picked up and made up intermediate riser joint #7. Ran in hole with high pressure drilling riser from 50m to 64m." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 92m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Picked up and made up double intermediate riser joint #3 and #6. Ran in hole with high pressure drilling riser from 64m MD to 92m MD." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 92m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Waited on crane due to handling of boat." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up and made up splash zone joint and upper pup joint. Ran in hole with high pressure drilling riser from 92m MD to 109m MD." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Changed to side door elevators for lifting tension joint." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 114m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up and made up riser tension joint. Ran in hole with high pressure drilling riser from 109m MD to 114m." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 114m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Observed crack on flange protector. Cargo strapped cracked protector." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Continued running in hole with high pressure drilling riser from 114m MD to 121m MD." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed side door elevators. Installed auto elevators and rotating arm." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Picked up and made up BOP joint with claxton NT2 running tool. Changed flange faces, cleaned and inserted gasket." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up riser. Removed elevators and C-plate. Removed riser spider." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Installed outer ring and master bushings." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to land high pressure drilling riser." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up x-over and 1 stand of drill pipe. Made up same to claxton running tool. Meanwhile: ROV removed debris cap from well head." "On 2013-08-01, at Well NO 15/9-F-1, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Ran in with riser from 121m MD to above riser guide funnel at 136m." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Ran in hole with riser from 136m to 137m. Entered riser guide funnel. Continued running in from 137m to top of wellhead. Rigged up tugger from moonpool to remove riser guide funnel." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Connected tugger to guide funnel and released hatch lock to disconnect riser guide funnel." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lowered hotstab connector to seabed. Removed dummy stab and installed hotstab. Switched connector valves to run-position." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Landed connector on wellhead and set down 20MT weight. Pressured up to 3000 psi until indicator rods in closed position." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Performed pull test by applying 15MT overpull on riser - ok. Filled riser while venting through open outlet on claxton tool." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared to install centralizers, tension ring and cylinders. Meanwhile: Lined up to pressure test well with cement unit. Performed line test to 100 bar for 10 minutes - ok. Built scaffolding around riser. Installed cap on claxton waco outlet." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: Installed centralizers and boat collision tool." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pressure tested riser and connector to 100 bar for 10 minutes - ok. Pumped a total of 1200 liters, bled 1200 liters back." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 8.2 hours. Operational details: Installed tension ring and cylinders." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Tranferred riser weight to cylinders. Tensioned up riser to 150MT." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleaned and tidied well head area and prepared to disengage claxton tool." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to disengage claxton tool." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Spotted claxton control reel on drill floor. Installed control wire sheave. Meanwhile: Changed fittings on claxton tool." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Rigged up air hoses to claxton control line reel. Ran hoses through rotary and installed same on claxton tool." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Set down 5MT on claxton tool. Pressure up and disengaged claxton running tool. Picked up same and installed split bushings. Set claxton tool in slips. Broke out stand and racked back in derrick." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up and made up pup joint to claxton tool. Removed outer bushings and outer ring. Picked up claxton tool to clear of rotary." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed outer ring and bushings." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to lay out claxton tool." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Broke out pup joint and laid out claxton tool to cantilever." "On 2013-08-02, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Prepared to nipple up BOP. Rigged up to pressure test IBOPs. Modified scaffolding in moonpool." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to nippling up BOP." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Moved BOP to well centre." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Nippled up BOP. Meanwhile: Pressure tested hoses and IBOPs." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to rigging up slick joint and diverter." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Rigged up slick joint. Attempted to lower diverter on to slick joint - no go. Found skid position not aligned." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Checked and adjusted pressure on tension cylinders and attempted to move slick joint under diverter - no go. Slacked off BOP on BOP craddle to fit BOP and slick joint below diverter - no go." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Prepared cantilever and deck equipment for skidding. Removed staires and bridge." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to perform skidding operation." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Skidded cantilever 20cm starboard. Verified alignment." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Lowered diverter on to slick joint. Not able to land correctly." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Pulled out diverter and checked same. Observed damage to alignment key on diverter. Removed alignment key and filed same to proper condition. Installed alignment key on diverter." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Landed off diverter. Installed hoses and activated diverter packer and overshot packer." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Filled up riser and BOP with seawater and verified no leaks." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Rigged down diverter running slips and shackles. Installed auto slips and rotating arm." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up and made up BOP test tool. Ran in hole to 139m and landed off in wellhead." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lined up to pressure test from cement unit. Closed upper pipe ram." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pressure tested BOP and riser to 345 bar for 10 minutes - ok. Pumped 389 liters, bled back 386 liters." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled out of hole with BOP test tool and laid down same to cantilever." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up and make up bore protector running tool." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up and made up bore protector running tool. Ran in hole with bore protector running tool on 5 1/2' drill pipe and set bore protector in wellhead by applying 5MT weight." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Released bore protector running tool by rotating one turn clockwise. Pulled out of hole with bore protector running tool on 5 1/2' drill pipe. Laid bore protector running tool out to deck." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleaned and tidied rig floor." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed prejob meeting prior to pick up and make up 17 1/2' bottom hole assembly." "On 2013-08-03, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Picked up and made up 17 1/2' bottom hole assembly to 50m." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Picked up and made up 17 1/2' bottom hole assembly from 50m to 109m." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed to 5 1/2' handling equipment." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Ran in hole with 17 1/2' bottom hole assembly on 5 1/2' heavy weight drill pipe from 109m to 230m." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Ran in hole with 17 1/2' bottom hole assembly on 5 1/2' drill pipe from 230m to 1000m." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Performed choke drill with both crews." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1281m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Ran in hole with 17 1/2' bottom hole assembly on 5 1/2' drill pipe from 1000m MD to 1281m MD." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1321m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Engaged top drive. Washed in hole from 1281m MD to 1321m MD. Tagged hard cement at 1321m MD with 10MT." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled cement in shoetrack from 1321m MD to 1348m MD with 3800 lpm, 120 bar, 60-80 rpm and 8-16 kNm. Drilled and reamed through shoe and rat hole from 1348m MD to 1355m MD. Displaced hole to 1.40 sg oil based mud while drilling shoe track." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 3 meters of new formation from 1355m MD to 1358m MD with 4200 lpm, 229 bar, 60 rpm and 7-11 kNm." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1358m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated and conditioned mud prior to perform FIT with 4200 lpm and 227 bar." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1358m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.2 hours. Operational details: Closed upper pipe rams. Performed FIT to 1.55 sg at 1358m MD with 1.40 sg oil based mud by applying 22 bar." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1440m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled and oriented 17 1/2' hole from 1354m MD to 1440m MD with 3800-4100 lpm, 150-228 bar, 120 rpm, 9-15 kNm, 1.41 sg ECD. Drilling ROP: 35 m/hr." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1440m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Observed 20MT overpull when picking up pipe for connection. Reamed area with 4100 lpm, 225 bar, 60 rpm and 9-11 kNm." "On 2013-08-04, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1510m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 1440m MD to 1510m MD with 4100-4400 lpm, 228-257 bar, 120 rpm, 8-15 kNm, 1.41 sg ECD. Drilling ROP: 35 m/hr." "On 2013-08-05, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1527m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 1517m MD to 1527m MD with 4400 lpm, 259 bar, 120 rpm, 10-13 kNm, 1.41 sg ECD. Drilling ROP: 35 m/hr. At 1517m MD, observed plugged line from swaco cuttings unit to boat." "On 2013-08-05, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1527m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed slow circulation rates. Meanwhile: Moved boat from port side to starboard side. Hooked up line from swaco cuttings unit to boat." "On 2013-08-05, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1527m. The activity was categorized as 'interruption -- other' and lasted for 15.0 hours. Operational details: Attempted to start-up transfer of cuttings on starboard side - no go. Starboard side hose plugged. Laid out port side hose to deck. Worked on cleaning out plug on port side hose. Meanwhile: Reciprocated pipe with 3000-4400 lpm, 131-257 bar and 100-120 rpm. Racked back one stand every hour. Reamed area from 1515m due to 10MT overpull. Reset V-ICIS system. Laid down 3 1/2' drill pipe to deck. Rigged up for racking back 13 3/8' casing in derrick. Performed general maintanence and housekeeping." "On 2013-08-05, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1623m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled and oriented 17 1/2' hole from 1527m MD to 1623m MD with 4500 lpm, 270 bar, 120 rpm, 12-18 kNm, 1.41 sg ECD. Drilling ROP: 35-40 m/hr At 1623m MD, observed plugged line from CCB to ISO-tanks." "On 2013-08-05, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1623m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed slow circulation rates. Meanwhile: Routed cuttings to skips on deck. Racked 13 3/8' casing in derrick." "On 2013-08-05, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1623m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Cleaned out plugged hose from CleanCut blower (CCB) to ISO-tanks. Meanwhile: Reciprocated pipe with 3600 lpm, 192 bar and 100 rpm. Performed general maintanence. Racked 13 3/8' casing in derrick." "On 2013-08-06, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1623m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Continued cleaning out hose from CCB funnel to ISO-tanks. Cleaned out plugged pressure sensors on CCB. Meanwhile: Racked 13 3/8' casing in derrick." "On 2013-08-06, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2047m. The activity was categorized as 'drilling -- drill' and lasted for 18.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 1623m MD to 2047m MD with 4400 lpm, 259-282 bar, 120-140 rpm, 10-23 kNm, 8-16 MT, 1.41-1.42 sg ECD. Drilling ROP: 25-30 m/hr." "On 2013-08-06, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2047m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed slow circulation rates." "On 2013-08-06, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2054m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2047m MD to 2054m MD with 4400 lpm, 282 bar, 140 rpm, 11-18 kNm, 10-16 MT and 1.41 sg ECD. Drilling ROP: 25 m/hr At 2054m MD, observed shut down of mud pumps." "On 2013-08-06, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2062m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and oriented 17 1/2' hole from 2054m MD to 2062m MD with 2000-4000 lpm, 80-243 bar, 140 rpm, 9-12 kNm, 2-4 MT and 1.40-1.41 sg ECD. Drilled with reduced ROP due to pump problems. Meanwhile: Troubleshot mud pumps. Electronic pop-off tripping at low pressures." "On 2013-08-06, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2087m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled and oriented 17 1/2' hole from 2062m MD to 2087m MD with 4400 lpm, 266-267 bar, 140 rpm, 15-23 kNm, 14-18 MT and 1.41 sg ECD. Drilling ROP: 25 m/hr" "On 2013-08-07, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2127m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled and oriented 17 1/2' hole from 2087m MD to 2127m MD with 4400 lpm, 266 bar, 140 rpm, 12-25 kNm, 10-16 MT and 1.41 sg ECD. Drilling ROP: 30 m/hr Observed areas with high torque due to calcareous stringers." "On 2013-08-07, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2127m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Observed overtorqued connection. Attempted to break connection and broke off connection on top of saver sub instead. Greased lower IBOP connection, increased make up torque and made up saver sub to lower IBOP. Broke connection and made up new stand." "On 2013-08-07, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2325m. The activity was categorized as 'drilling -- drill' and lasted for 12.5 hours. Operational details: Drilled and oriented 17 1/2' hole from 2127m MD to 2325m MD with 4400 lpm, 266 bar, 120-160 rpm, 12-30 kNm, 16-20 MT and 1.41 sg ECD. Reamed 1 single at 2207 m MD prior to connection. Reamed 1/2 single at 2249 m MD prior to connection. Reamed 1/2 single at 2290 m MD prior to connection. Drilling ROP: 16 m/hr Observed areas with high torque due to calcareous stringers." "On 2013-08-07, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2325m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Recorded SCR's prior to connection." "On 2013-08-07, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2369m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2325 m MD to 2369 m MD with 4400 lpm, 266 bar, 120-160 rpm, 12-30 kNm, WOB 11-19 Ton, 1,40 - 1,41 sg ECD. Average drilling ROP 25 m/hr." "On 2013-08-07, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2369m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Not able to brake out over torqued DP connection. Attempted to break connection, saver sub / lower IBOP connection broke unintended. Made up saver sub / lower IBOP connection, increased make up torque to 80000 ft/lbs. Broke out DP connection and made up new stand." "On 2013-08-07, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2438m. The activity was categorized as 'drilling -- drill' and lasted for 6.2 hours. Operational details: Drilled and oriented 17 1/2' hole from 2369 m MD to 2438 m MD with 4430 liter/min, 282 - 292 bar, 140-160 rpm, 15-24 kNm, WOB 15-20 Ton, 1,39 - 1,41 sg ECD. Average drilling ROP 11 m/hr." "On 2013-08-08, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2602m. The activity was categorized as 'drilling -- drill' and lasted for 21.8 hours. Operational details: Drilled and oriented 17 1/2' hole from 2438 m MD to 2602 m MD with 4430 liter/min, 280 - 290 bar, 90-140 rpm, 16-27 kNm, WOB 15-20 Ton, ROP 3-18 m/h, 1,39 - 1,41 sg ECD. Average drilling ROP 7,5 m/hr Meanwhile picked up and racked back 13 3/8' casing in derrick." "On 2013-08-08, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2602m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Reciprocated string while circulating hole clean with 4365 l/min, 275-280 bar, 120 rpm, 5-9 kNm, ECD 1,391 sg. Racked back 1 stand after 1 x bottoms up." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2602m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Reciprocated string while circulating hole clean with 4365 l/min, 275-280 bar, 120 rpm, 5-9 kNm. Racked back 1 stand after each bottoms up. Observed fair amount of cuttings coming across shakers after 3 x bottoms up. Observed minor amount of cuttings coming across shakers after 4 x bottoms up. Circulated total 4 x bottoms up." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2490m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Performed downlink. Recorded up down weights 163 / 137 Ton." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2490m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Flow checked well for 10 minutes, ok." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2329m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POOH wet with 17 1/2' BHA on 5 1/2' DP from 2490 m to 2329 m." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2329m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 5 m3 1,74 sg slug and chased same with 1,4 sg OBM. Not able to commence tripping due to faulty finger in finger board." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2329m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Repaired finger in DP finger board." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1326m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 2329 m to 1326 m. Restricted tripping speed to 1 min/stand." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1326m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well for 10 minutes inside 20' shoe, ok. Meanwhile performed pre-job meeting. Serviced TDS and checked dolly rollers." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1042m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 1326 m to 1042 m. Restricted tripping speed to 1 min/stand. Stopped tripping due to encoderfailure on Aft PRS." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1042m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Troubleshoot Aft PRS and reset same, not able to eliminate encoder failure. Continued tripping using fwd PRS." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 1042 m to 136 m." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 10 minutes prior to pull through BOP's, ok. Meanwhile performed pre-job meeting prior to lay down BHA." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Removed PS-21 and installed master bushings. POOH with 17 1/2' BHA from 136 m to 24 m and laid down same to cantilever." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Plugged into MWD tool and down loaded data." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 17 1/2' BHA from 24 m to surface and laid down same to cantilever. Cleaned and cleared drill floor." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: Picked up and made up bull nose and seat protector RRT assembly. RIH with assembly on 5 1/2' HWDP and jet washed BOP area. Continued to RIH with assembly to NSP area and jet washed same. Engaged and retrieved seat protector. Pulled free with 12 Ton overpull. New datum 138,86 meter. Jet washed NSP area. Dropped 2 7/8' drift. POOH with assembly and laid down same. Cleaned and cleared drill floor." "On 2013-08-09, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Rigged up bails and BX elevators for 13 3/8' casing." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Installed casing fill up tool on TDS. Removed master bushings and installed FMS. Installed 13 3/8' casing tong." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to run 13 3/8' casing." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up shoe track from derrick, made up to double, Baker locked connection and RIH to 63 m. Experienced problems with running centralizers through slips, removed guides on slips and filled string to enable centralizers to run through." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 210m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 13 3/8' casing in stands from 63 to 210 m. Filled casing every 2.th stand." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 210m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Experienced problems with casing tong, not able to release grip." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 308m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 13 3/8' casing in stands from 210 to 308 m. Filled casing every 2.th stand." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 308m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Installed guides in slips. Held pre-job meeting with oncoming crew prior to run casing." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 504m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with 13 3/8' casing in stands from 308 m to 504 m. Filled casing every 3.th stand. Average running speed 112 m/hr - 9 joint/hr." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 504m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Attempted to adjust casing fill up tool to enable filling while RIH, not applicable." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: RIH with 13 3/8' casing in stands from 504 m to 1348 m. Filled casing every 3.th stand. Average running speed 153 m/hr - 13 joint/hr." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1348m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Engaged casing fill up tool and broke circulation. Circulated for 10 minutes with 400-1200 liter/min, 10-16 bar." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2155m. The activity was categorized as 'drilling -- casing' and lasted for 6.5 hours. Operational details: RIH with 13 3/8' casing in stands from 1348 m to 2155m. Filled casing every 3.th stand. Average running speed 125 m/hr - 10 joint/hr." "On 2013-08-10, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2228m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 13 3/8' casing in stands from 2155 m to 2228 m. Worked tight spots between 2155 m - 2165 m, 2195 m - 2200 m. Filled casing every 3.th stand." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2448m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 13 3/8' casing in stands from 2228 m to 2448 m. Filled casing every 3.th stand. Average running speed 110 m/hr - 9 joint/hr." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2448m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rigged down casing fill up tool, bails and casing elevator. Rigged up 5 1/2' DP handling equipment." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2448m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up casing hanger." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2448m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed casing slips and installed master bushings." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2448m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed protection from hanger and checked seals. Hanger not able to pass through rotary due to misalignment." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2448m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rigged up snatch block to align hanger and allow it to pass through rotary." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2460m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Ran hanger through rotary and sat in manual slips." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2460m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged down 13 3/8' casing tong." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2570m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 13 3/8' casing on 5 1/2' HWDP landing string from 2460 m to 2570 m. Experienced tight spot between 2562 m - 2570 m. Worked tight spot, not able to pass 2570 meter." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2560m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made up TDS to string and established circulation with 500 liter/min, 18 bar." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- casing' and lasted for 8.2 hours. Operational details: Washed and worked down 13 3/8' casing on 5 1/2' HWDP landing string from 2560 m to 2596 m with 500-1500 liter/min, 18-45 bar, 20-40 Ton down weight. The hole packed off several times. Lost 500-3000 liter/hour to formation." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up and made up cement stand to landing string. Landed casing hanger in wellhead, sat down all weight. Rotated 1/4 right hand turn." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Established circulation and increased rate in steps to 2200 liter/min, 29 bar. Observed pack off at 2200 liter/min, reduced rate to at 1800 liter/min, 21 bar Meanwhile performed pre-job meeting prior to cement job. Rig air supply from production shut down." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'interruption -- repair' and lasted for 3.2 hours. Operational details: Production troubleshot on rig air system and consumption. Tested and confirmed air supply ok. Meanwhile: Pressure tested surface lines and cement hose to 30 / 345 bar - 5 / 10 minutes. Circulated and conditioned mud with 1800 liter/min, 21 bar." "On 2013-08-11, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Pumped 25 m3 of 1,75 sg spacer using rig pumps with 1560 liter/min, 15 bar. Lined up to pump from cement unit. Applied 20 bar pressure behind IBOP. Released dart for bottom wiper plug. Mixed and pumped 27,7 m3 of 1,90 sg cement slurry at 600 liter/min. Observed dart landing and shearing. Released dart for top wiper plug." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Displaced cement to rig floor with 3000 liter of drill water. Observed top wiper plug shear. Zeroed volume counters. Continued to displace cement using rig pumps with OBM at 1800 liter/min, 0-60 bar. Observed bottom wiper plug landing with 136 bar. Observed loss of full returns after 180 m3 pumped. Reduced rate to 1400 liter/min, still not full returns. Reduced rate to 500 liter/min after 181,5 m3 pumped. Displaced with theoretical volume + 1/2 shoe track volume 186,4 m3 + 1,25 m3 = 187,6 m3. Top plug did not bump. Recorded FCP 60 bar. Lost 10,2 m3 during cement displacement." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Bled off pressure and checked for back flow on cement unit. No back flow observed." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Set and pressure tested seal assembly to 345 bar / 15 min." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.5 hours. Operational details: Tested BOP pipe rams and annular to 20 / 345 bar - 5 / 10 minutes. Meanwhile performed pre-job meeting prior to break out and lay down cement head." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Released casing hanger RT. Broke out and laid down cement head. Installed 2 ea. sponge balls in string. Circulated clean with 2230 liter/min, 19 bar. POOH with casing hanger RT and laid down same." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor. Held pre-job meeting prior to wear bushing run." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed wear bushing in WH, datum at 138,92 meter." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Continued to test BOP pipe rams to 20 / 345 bar - 5 / 10 minutes." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Broke out and laid down jet sub / wear bushing RT assembly. Cleaned and cleared drill floor." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: Pressure tested IBOP's, kelly hose and manifolds to 20 / 345 bar - 5 / 10 minutes." "On 2013-08-12, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 6.0 hours. Operational details: Waited on cement. Meanwhile; Performed planned maintenence on TDS and travelling block. Restarted V-ICIS. Replaced wash pipe. Measured TDS / dolly alignment using laser equipment. Replaced solenoid valve on aft PRS" "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: Waited on cement. Meanwhile; Pressure tested manifolds to 20 / 345 bar - 5 / 10 minutes. Performed planned maintenence on TDS and travelling block. Installed BHA Wash Tool." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Pressure tested 13 3/8' casing to 20 / 320 bar - 5 / 10 minutes against blind shear ram." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 167m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Made up and RIH with 12 1/4' BHA from surface to 167 meter." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- trip' and lasted for 4.2 hours. Operational details: RIH with 12 1/4' BHA on 5 1/2' DP from 167 m to 2508 m. Average tripping speed 550 m/hr - 13 stds/hr. Filled pipe every 1000 meter." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2508m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Performed choke drill." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2548m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Established circulation and washed down with 12 1/4' BHA on 5 1/2' DP from 2508 m to 2548 m at 2000 liter/min, 82 bar. Tagged TOC at 2548 meter." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2605m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled shoetrack and cement from 2548 m to 2602 m with 2000 - 2500 liter/min, 85-122 bar, 30-60 rpm, 8-20 kNm, WOB 3-11 Ton. Reduced mud weight from 1,40 sg to 1,28 sg OBM while drilling. Cleaned out rat hole in 1-2 meter steps, reamed rat hole twice. Meanwhile prepared for pick up and racking of 10 3/4' casing." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2605m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 3 meter new formation to 2605 meter. Pulled back into shoe without circulation or rotation to confirm no restrictions observed." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2605m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated and conditioned mud until 1,28 sg mud in and out with 3000 liter/min, 145 bar. Meanwhile lined up and tested lines from cement unit to 120 bar / 5 min" "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2605m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.2 hours. Operational details: Performed FIT to 66 bar using 1,28 sg mud, 1,55 sg EMW. Pumped 877 liter from 5 bar to 66 bar at cement unit with 55 liter/min. Bled back 811liter." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2605m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.5 hours. Operational details: Flow checked well for 10 min, OK." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2601m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Dropped gyro. Waited for gyro to initialize." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 4 m3 1,56 sg slug with 1000 liter/min, 22 bar." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 436m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 2590 m to 436 m. Average tripping speed 957 m/hr." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 436m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Made up string and took orientation shots." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 167m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 436 m to 167 m. Average tripping speed 1076 m/hr." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 167m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 10 min, OK. Meanwhile removed PS-21 slips and installed master bushings." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' HWDP from 167 m to 97 m. Not able to retrieve gyro due to wrong retrival tool setup." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 99m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Reconfigured gyro retrieval tool." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 99m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Retrieved gyro." "On 2013-08-13, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 12 1/4' BHA from 97 m to surface and laid down same. Cleaned and cleared drill floor." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed Pre-job Meeting prior to make up 8 1/2' BHA. Changed to 5' handling equipment." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 151m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: Picked up and made up 8 1/2' drilling BHA and RIH from surface to 151 meter." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1011m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' HWDP / DP from 151 m to 1011 m. Average tripping speed 688 m/hr." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1011m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Tested MWD tools with 2000 liter/min, 118 bar." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2585m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' HWDP / DP from 1011m to 2585 m. Average tripping speed 787 m/hr. Filled pipe every 1000 meter." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2605m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Washed down from 2585 m to 2605 m with 1800 liter/min, 111 bar, 60 rpm, 9-13 kNm." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2779m. The activity was categorized as 'drilling -- drill' and lasted for 7.8 hours. Operational details: Drilled and oriented 8 1/2' hole from 2605 m MD to 2779 m MD with 1990 - 2389 liter/min, 142 - 207 bar, 60-130 rpm, 11-19 kNm, WOB 5-10 Ton, ROP 37-42 m/h, 1,31 - 1,34 sg ECD. Average drilling ROP 23 m/hr Meanwhile picked up and racked back 10 3/4' casing in derrick." "On 2013-08-14, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2905m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled and oriented 8 1/2' hole from 2779 m MD to 2905 m MD with 2400 - 2470 liter/min, 207 - 211 bar, 130-160 rpm, 17-21 kNm, WOB 5-12 Ton, ROP 39-18 m/h, 1,34 - 1,35 sg ECD. Average drilling ROP 24 m/hr Meanwhile picked up and racked back 10 3/4' casing in derrick." "On 2013-08-15, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3145m. The activity was categorized as 'drilling -- drill' and lasted for 11.2 hours. Operational details: Drilled and oriented 8 1/2' hole from 2905 m MD to 3145m MD with 2450 - 2570 liter/min, 202 - 216 bar, 160 rpm, 18-21 kNm, WOB 4-12 Ton, ROP 18-25 m/h, 1,35 - 1,37 sg ECD. Average drilling ROP 21 m/hr Meanwhile picked up and racked back 9 5/8' casing in derrick." "On 2013-08-15, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3145m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Recorded SCR's" "On 2013-08-15, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3253m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3145 m MD to 3253 m MD with 2570 - 2707 liter/min, 205 - 214 bar, 160 rpm, 17-23 kNm, WOB 4-8 Ton, ROP 18-25 m/h, 1,37 - 1,39 sg ECD. Average drilling ROP 22 m/hr Increased MW from 1,28 sg to 1,32 sg while drilling. Meanwhile picked up and racked back 9 5/8' casing in derrick." "On 2013-08-15, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3253m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Pulled off bottom and trouble shoot Sonic tool failure. Sonic tool not fuctional." "On 2013-08-15, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3364m. The activity was categorized as 'drilling -- drill' and lasted for 7.2 hours. Operational details: Drilled and oriented 8 1/2' hole from 3253 m MD to 3364 MD with 2446 - 2570 liter/min, 205 - 213 bar, 160 rpm, 18-23 kNm, WOB 4-8 Ton, ROP 11-22 m/h, 1,38 - 1,39 sg ECD. Average drilling ROP 15 m/hr Meanwhile picked up and racked back 9 5/8' casing in derrick. Total 44 stands racked back." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3450m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Drilled and oriented 8 1/2' hole from 3364 m MD to 3450 MD with 2389 - 2565 liter/min, 208 - 216 bar, 160 rpm, 17-23 kNm, WOB 4-10 Ton, ROP 9-23 m/h, 1,39 - 1,40 sg ECD. Average drilling ROP 16 m/hr Meanwhile picked up and racked back 9 5/8' casing in derrick." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3591m. The activity was categorized as 'drilling -- drill' and lasted for 8.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3450 m MD to 3591 m MD with 2389-2435 liter/min, 213 - 220 bar, 160 rpm, 18-23 kNm, WOB 3-5 Ton, ROP 5-20 m/h, 1,39 - 1,40 sg ECD. Average drilling ROP 18 m/hr Meanwhile picked up and racked back 9 5/8' casing in derrick." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3591m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Recorded SCR's." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled and oriented 8 1/2' hole from 3591 m MD to 3632 m MD with 2389 liter/min, 218 - 220 bar, 160 rpm, 17-22 kNm, WOB 3-5 Ton, ROP 5-20 m/h, 1,39 sg ECD. Average drilling ROP 14 m/hr Meanwhile picked up and racked back 9 5/8' casing in derrick." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.2 hours. Operational details: Circulated hole clean with 2400 liter/min, 218 bar, 142 rpm, 17-19 kNm. Circulated total 2 1/2 x bottoms up." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Flow checked well for 10 minutes, OK." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3496m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pumped OOH from 3632 m to 3496 m with 2450 liter/min, 200 bar." "On 2013-08-16, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3496m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: Attempted to take pressure points. No communication with tool." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3390m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Run back to bottom. POOH wet with 8 1/2' BHA on 5 1/2' DP from 3632 m to 2450 m. Performed pre-job meeting prior to re-logging for 15 minutes." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3349m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: Re-logged interval from 3390 m to 3349 m with 2450 liter/min, 210 bar, 90 rpm, 12-21 kNm." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 3349 m to 3632 m." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: Filled pipe, observed pressure increase, worked string clear. Circulated with 2450 liter/min, 215 bar, 140 rpm, 12-19 kNm." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Dropped gyro and pumped down same with 500 liter/min, 20 bar, 20 rpm, 12-18 kNm." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- pressure detection' and lasted for 0.2 hours. Operational details: Flow checked well for 10 minutes, OK." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2706m. The activity was categorized as 'drilling -- trip' and lasted for 5.2 hours. Operational details: POOH wet with 8 1/2' BHA on 5 1/2' DP from 3632 m to 2706 m. Worked tight spots at 3472, 3126, 3075, 3064, 3028 meter. Restricted pulling speed 2 min/stand. Took gyro readings / shoots." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2706m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Pumped 4 m3 1,56 sg slug with 1000 liter/min, 22 bar." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP from 2706 m to 2596 m. Restricted pulling speed 2-1 min/stand. Took gyro readings / shoots." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2596m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 10 min, OK." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 203m. The activity was categorized as 'drilling -- trip' and lasted for 4.2 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP from 2596 m to 203 m. Took gyro readings / shoots as required" "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 203m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well for 10 min, OK. Held pre-job meeting prior to handling BHA." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 206m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Retrieved Gyro from string." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' HWDP / DC from 203 m to 52 m. Racked back / laid down BHA." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to handling radioactive source." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 52m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Removed radioactive source from BHA." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held pre-job meeting for 15 minutes. POOH and broke down 8 1/2' BHA from 52 m to 45 m." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Down loaded data from MWD tool." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH and broke down 8 1/2' BHA from 45 m to surface." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor." "On 2013-08-17, at Well NO 15/9-F-1, a drilling event occurred at a depth of 21m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: Picked up and made up 8 1/2' BHA, RIH from surface to 21 meter." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 44m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Picked up and made up 8 1/2' BHA, RIH from 21 m to 44 m." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 44m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Plugged into MWD and initialized same." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 190m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Picked up and made up 8 1/2' BHA, RIH from 44 m to 190 m." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 190m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed master bushings and installed PS-21 power slips." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 997m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' HWDP / DP from 190 m to 997 m. Average tripping speed 807 m/hr." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 997m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Filled pipe and shallow tested MWD tools at 2400 liter/min, 121bar." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1800m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 997 m to 1800 m. Average tripping speed 803 m/hr." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1800m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Emtied trip tank and filled pipe." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2571m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 1800 m to 2571 m. Average tripping speed 771 m/hr." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2571m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Filled pipe." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2571m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting prior to slip & cut." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2571m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Rigged up, slipped and cut drill line. Calibrated block after slip & cut." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2936m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 2571 m to 2936 m. Reduced speed due to hole condition." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2976m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Washed and reamed tight spot between 2936 m and 2976 m with 2000 liter/min, 120 bar, 80 rpm, 8-16 kNm." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3215m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 2976 m to 3215 m. Reduced speed due to hole condition." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3215m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Washed and reamed tight spots between 3175 m and 3215 m with 2000 liter/min, 121 bar, 80 rpm, 8-16 kNm." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3264m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 3215 m to 3264 m. Reduced speed due to hole condition." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'interruption -- repair' and lasted for 3.8 hours. Operational details: Washed and reamed string down from 3264 m to 3632 m with 1000 liter/min, 44 bar, 50 rpm, 8-13 kNm. At 3286 m hole packed off, stopped pumps and slided through obstruction." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3620m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Circulated hole clean with 2450 liter/min, 185 bar, 130-150 rpm, 14-19 kNm. Reciprocated string. Circulated total 3 x bottoms up." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3620m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Flow checked well for 10 min, OK." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3499m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: POOH wet with 8 1/2' BHA on 5 1/2' DP from 3620 m to 3499 m." "On 2013-08-18, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3347m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Recorded pressure points." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3347m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Recorded pressure points." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3620m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' BHA on 5 1/2' DP from 3347 m to 3620 m. Reduced speed due to hole condition." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3333m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.2 hours. Operational details: Back reamed OOH while re-logging from 3620 m to 3333 m with 2540 liter/min, 170 bar, 100 rpm, 12-22 kNm." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3295m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: Observed tight spot at 3333 meter, attempted to work through without rotation. Hole packed off. Pulled back to 3295 without flow. Ran back in to 3335 with 1650 liter/min, 87 bar. Re-logged stand from 3333 m to 3295 m." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3255m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.2 hours. Operational details: Pumped OOH from 3295 m to 3257 m, experienced tight hole. Ran back in to 3273 m without circulation. Re-logged stand from 3273 m to 3255 m." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2652m. The activity was categorized as 'formation evaluation -- log' and lasted for 9.0 hours. Operational details: Back reamed OOH while re-logging from 3255 m to 2652 m with 2540 liter/min, 160-168 bar, 100-120 rpm, 11-21 kNm." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2584m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: POOH while re-logging from 2652 m to 2584 m with 2540 liter/min, 160-168 bar." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2584m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.2 hours. Operational details: Circulated bottoms up with 2430 liter/min, 218 bar, 130 rpm." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2584m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: Flow checked well, OK." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2584m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Function tested BOP." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2584m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 4 m3 1,56 sg slug with 1000 liter/min, 22 bar." "On 2013-08-19, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1800m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP from 2584 m to 1800 m. Average tripping speed 784 meter/hr." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 877m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP from 1800 m to 877 m. Average tripping speed 723 meter/hr. Stopped due to fault on iron roughneck." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 877m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Repaired electical failure on iron roughneck. Meanwhile observed well on trip tank." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' DP from 877 m to 190 m. Average tripping speed 916 meter/hr." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well for 10 min, OK." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 8 1/2' BHA on 5 1/2' HWDP from 190 m to 43 m. Laid down jar and accelerator." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Changed handling equipment." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 43m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.8 hours. Operational details: Plugged into MWD tool and down loaded data." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued laying down BHA from 43 m to surface" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Cleaned and cleared rig floor after L/D BHA. Changed handling gear in IR and BX elevator. Removed master bushing and installed PS 21. Moved rollers on cantilever." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Picked up 3 1/2' DP singles, made up and RIH open ended from surface to 143 m." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 143m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Experienced bad connection, checked threads, cleaned box and pin. Retried to M/U - no success. Layed out two singles of 3 1/2' DP" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 325m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Continued P/U 3 1/2' DP singles and RIH from 143 m to 325 m" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 325m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed handling equipment from 3 1/2' to 5 1/2'" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: RIH w/ cement stinger on 5 1/2' DP from 325 m to 2550 m . Avg. tripping speed 1270 m/hr." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2550m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Broke circulation at 2550 m. Staged up flow and circulated w/ 2450 l/min, 170 bar" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3154m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: RIH in open hole from 2550 m to 3154 m, restricted running speed due to open ended stinger. Avg. tripping speed 400 m/hr" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3154m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke circulation at 3154 m. Circulated w/ 1330l/min, 60 bar" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3594m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Cont. RIH in open hole from 3154 m to 3594 m. Restricted running speed due to open ended stinger." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Established circulation and washed down last stand with 500 lpm, 20 bar. Tagged bottom at 3632 m." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Staged up pumps to 2500 lpm , 190 bar. Circulated hole clean. Reciprocated and rotated pipe with 60 - 120 rpm while circulating." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Layed out one single. P/U and M/U cement assy. Connected cement hose" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Established circulation, circulated B/U prior to cement job with 2450 lpm, 187 bar. Performed TBT for setting cement plug #1" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Balanced cement plug #1 (3632 m - 3353 m ): Pumped 11,8 m3 of 1,60 SG spacer, 800 l/min/ 30 bar. Mixed and pumped 13,3 m3 of 1,90 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Zeroed volume counters. Pumped 5,2 m3 of 1,60 SG spacer. Displaced the cement with 31,6 m3 (1455 strokes) of 1,32 SG OBM, 2450 l/min/ 180 bar at 30 RPM." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Broke off cement line, layed out cement assy." "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3350m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pulled out of cement to 3350 m MD. Restricted speed to 3 min/stand" "On 2013-08-20, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3350m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Made up TDS and circulated out excess cement, 2450 lpm, 200 bar, 80 rpm, 12 kNm." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3350m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Circulated out excess cement, 2450 lpm, 200 bar, 80 rpm, 12 kNm. Performed TBT for setting cement plug #2" "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3350m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: M/U cement assy and installed cement hose. Tested line to 200 bar for 5 min" "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3350m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Balanced cement plug #2 (3350 m - 3074 m ): Pumped 11,8 m3 of 1,60 SG spacer, 800 l/min/ 29 bar. Mixed and pumped 13,3 m3 of 1,90 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water. Zeroed volume counters. Pumped 5,2 m3 of 1,60 SG spacer. Displaced the cement with 28 m3 (1290 strokes) of mud, 2450 l/min/ 114 - 170 bar at 30 RPM." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Broke off cement hose, layed out cement assy. Pulled out of cement to 3070 m. Restricted pulling speed to 3 min/stand" "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- other' and lasted for 2.2 hours. Operational details: Circulated out excess cement, 2450 l/min/ 188 bar at 80 rpm, 12 kNm." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Circulated and conditioned mud prior to setting cement plug #3 and mixed new spacer." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Rigged up cement assy, installed cement hose and positioned string at 3070 m" "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- other' and lasted for 1.2 hours. Operational details: Balanced cement plug #3 (3070 m - 2795 m ): Pumped 11,8 m3 of 1,60 SG spacer, 600 l/min/ 10 - 25 bar. Mixed and pumped 13,3 m3 of 1,90 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water. Zeroed volume counters. Pumped 5,2 m3 of 1,60 SG spacer. Displaced the cement with 25,1 m3 (1156 strokes) of mud, 2500 l/min/ 100 - 155 bar at 25 RPM." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Layed out cement assy." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2790m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pulled out of cement to 2790 m MD. Restricted pulling speed to 2 - 3 min/stand" "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2790m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Circulated out excessive spacer and cement at 2790 m, 2500 lpm, 172 bar, 80 rpm." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2790m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Made up cement assy, installed cement hose, positioned string at 2790 m. Confirmed line-up." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2790m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Cement/KO plug #4 (2790 m - 2545 m ): Pumped 11,8 m3 of 1,60 SG spacer, 800 l/min/ 10 - 25 bar. Mixed and pumped 13,4 m3 of 2,00 SG cement slurry, 600 l/min. Displaced the cement to the rig floor with 890 l of drill water. Zeroed volume counters. Pumped 1,3 m3 spacer. Displaced the cement with 26,8 m3 (1234 strokes) of mud, 2500 l/min/ 140 - 170 bar at 25 RPM." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Pulled out of cement to 2590 m. Restricted pulling speed to 2 - 3 min/stand." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Installed sponge balls, circulated out excessive cement and hole clean, 2500 lpm, 170 - 180 bar at 60 - 120 rpm. Reciprocated string." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Well static." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Pumped slug" "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2180m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: POOH w/ 3 1/2' cement stinger on 5 1/2' DP from 2590 m to 2180 m . Avg. tripping speed 820 m/hr." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2180m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Carriage travel fault on iron roughneck, identified faulty cable, rectified and secured same" "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 326m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: POOH w 5 1/2' DP from 2180 m to 326 m . Avg. tripping speed 927 m/hr." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 326m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Well static. Meanwhile changed handling equipment from 5 1/2' to 3 1/2'." "On 2013-08-21, at Well NO 15/9-F-1, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: L/D 34 joints of 3 1/2 DP, 26 jnts/hr." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: RIH 26 5 1/2' DP stands from derrick" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Installed sponge balls, made up TDS and circulated 3x string volume w/ 2500 l/min, 29 bar" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: POOH stands and racked same" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Cleanend and cleared rig floor, changed handling gear" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre- job meeting for handling BHA" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: P/U and M/U BHA as per Baker DD instructions. Broke out 8 3/8' flex stab from ASS stearing head. P/U module #1 and changed bit." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed pre-job meeting with upcoming shift" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: P/U and M/U BHA in modules as per Baker DD instructions" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Plugged into tools and verified same, took scribe line from OnTrak to TesTrak. M/U X/O, float sub and string stab." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Placed barriers, made announcement for handling radioactive sources. RPS installed sources." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 198m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Continued P/U and M/U BHA as per Baker instructions" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 198m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Installed PS 21 slips" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: RIH w/ 8 1/2' BHA on 5 1/2' DP from 198 m to 1000 m . Avg. tripping speed 641 m/hr." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Filled pipe and tested MWD tools w/ 2180 lpm and 118 bar." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1814m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Continued RIH with 5 1/2' DP from 1000 m to 1814 m." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 1814m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Filled pipe at 1814 m." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2539m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH 5 1/2' DP from 1814 m to 2539 m . Avg. tripping speed 967 m/hr." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2592m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Filled pipe, washed from 2539 m to 2592 m w/ 1770 l/min, 90 bar, 30 RPM, 8 kNm. Tagged cement with 2 tons, soft cement." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2590m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: Circulated and conditioned mud w/ 2450 l/min, 180 bar. Reduced MW from 1,32 SG to 1,28 SG. Reciprocated string while circ. Flushed all surface lines and took SCR with new mud weight. Meanwhile isolated and serviced all drillfloor equipment." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2598m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: M/U next stand and washed in through soft cement from 2592 m to 2598 m, 1800 lpm, 95 bar, 60 rpm, 8 kNm. Firm cement at 2598 m, 5 ton WOB. Pulled back into shoe to confirm string free." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2601m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled cement from 2598 m to 2601 m, WOB 2-3 tonne. 1800 l/min, 95 bar. 60 rpm / 8 - 15 kNm." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2601m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Reamed back through shoe, broke out double and racked same. M/U new stand to enable continues kick-off" "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2601m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Reamed to bottom at 2601 m w/ 1800 l/min, 95 bar, 60 RPM, 8 - 12 kNm. Observed string stall and pressure increase to 200 bar. Not able to rotate and circulate, pressure increases immediatly." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2601m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Stuck with flex stab in 13 3/8' shoe, stab 5 m behind bit. Attempted to free string and regaining circulation by working 40 kNm torque in string and keeping 60 bar pressure on string. Pressure dropping off and flow reported in flowline." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2601m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Worked torque out of string and took 100 t overpull to 150 t hockload. Attempted to cock jar down and pick up to 250 ton, jar did not fire. Attempted to cock jar and picked up to 300 ton on hook (150 t overpull). String was observed to be free. Pulled back into csg shoe." "On 2013-08-22, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2601m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: Worked string above shoe to clear BHA with 2500 lpm, 161 bar, 120 rpm, 6 - 15 kNm" "On 2013-08-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2602m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: Worked string in steps through shoe from 2592 m to 2601 m with 2500 lpm, 161 bar, 120 rpm, 6-25 kNm. String attempted to stall several time while working rathole. Oberserved pressure spikes while going to bottom. Worked area several times. Drilled to 2602 m." "On 2013-08-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2610m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Started to kick off from 2602 m. Send downlink to set tool in hold mode. Drilled from 2602 m to 2610 m, 2000 lpm, 113 bar, 80 rpm, 8 - 12 kNm, 2 - 4 tons WOB, Controlled ROP 5 m/h." "On 2013-08-23, at Well NO 15/9-F-1, a drilling event occurred at a depth of 2620m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Sent downlink to increase build force. Drilled 8 1/2' hole from 2610 m to 2620 m, WOB 4 tonne. 2000 l/min/ 116 bar. 80 rpm / 8 - 12 kNm. Controlled ROP 7 m/h. 50% Formation at 2620 m. Last report on F-1 - Continue to report on F-1A" "On 2007-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Skidded cantilever from F-5 to F-15." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.0 hours. Operational details: Re-established cantilever for operation. Removed hatches from F-15 at all levels in WH module." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk prior to make up 36' HO BHA." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 132m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Made up 36' HO BHA from rotary to 132m." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 144m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Stabbed 36' BHA into funnel and tagged seabed with 5 MT at 144.2m." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Attempted to wash down 36' BHA through template. Drilled 36' hole from 144 m to 149 m MD. Drilling parameters : Flow 1000 lpm / SPP 1-2 bar / 20 RPM / Torque 2-12 kNm / WOB 2-6 MT." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 149m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 36' hole from 147 m to 149 m MD. Drilling parameters : Flow 1000 lpm / SPP 4-5 bar / 20 RPM / Torque 3-10 kNm / WOB 1-3 MT. Drilling bushing landed out in template guide-funnel. Parked ROV in garage." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- drill' and lasted for 9.8 hours. Operational details: Drilled 36' hole from 149 m to 226 m MD. (17 1/2'' hole depth) Drilling parameters : Flow 3800-4700 lpm / SPP 52-82 bars / 90 RPM / Torque 2-9 kNm / WOB 2-6 MT / ROP 10-28 m/hr. Pumped 20m³ hi-vis pills prior to connection. Survey at 149.7 m 0.21 inc Survey at 160.2 m 0.04 inc Survey at 170.34 m 0.06 inc Survey at 180.09 m 0.09 inc Survey at 190.38 m 0.09 inc Survey at 200.41 m 0.19 inc Survey at 211.13 m 0.03 inc" "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated 1.5 bottoms up with sea water. Swept with 25 m³ Hi-Vis pill at max flow rate. Displace hole with 1.40 sg mud. 1.5 hole volume 80 m³ at max flow rate 4700 lpm 109 bars." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Held tool box talk prior to POOH with 36' HO BHA. POOH to 5 m below sea bed at 150m. Top up hole with 10m³ 1.40 sg mud. Continued pull out with 36' BHA. Racked back collars and MWD in derrick. Laid out 36' HO." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Laid out 36' HO. Inspected derrick for loose items. Cleared rig floor." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Serviced and inspected the TDS." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Rigged up for running 30' conductor." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box prior to run 30' conductor." "On 2007-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up 30' shoe joint, checked float for flow through by flushing with water." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continued checking the float for flow through by flushing with water." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 67m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Ran in with 30' conductor from surface to 67m." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 67m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Changed bails and 5½' DP elevator. Picked up 30'conductor housing." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 67m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to making up the 30' conductor housing. Commenced to make up 30' conductor housing using manual rig tongs." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Made up 30' conductor housing using manual rig tongs. Made Up Torque 46.000Nm. Engage locking system with lock-plate. Secured with cap-screws. Inspected housing. Lowered 30' housing down in the rotary. Broke out the 30' housing handling tool and laid out same. Filled 30' conductor with sea water." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk prior to pick up cement inner string. Made up aluminum cement inner string and centralizer. Cleared rig floor." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Made up X/O to CART, and then chained tong onto aluminium inner string. Installed inclinometer and 2' vent valve (valve open) on CART." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Locked CART housing as per Vetco instruction. 5 left hand turns. Took pick up test. Remove 30' housing C-plate. Ran conductor through rotary, and insert master bushing." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up to TDS and filled the 30' conductor with sea water. Commenced to stab shoe into to the slot. Stopped operation due to posiblity of power failure in production module." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 90m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Stopped operation due to possiblity of main shut down due to testing in prosess module." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Stabbed 30' conductor in to slot. Broke circulation and confirmed conductor to be full. Closed the 2' vent valve. Ran in with the 30' conductor from 144m to 220.6m" "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Verified setting depth with Digiquartz against F-7, F-15 -6/-9mm. Checked centralization of conductor housing, no contact to template. Meanwhile pressure tested cement line to 200 bars 10 min." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Checked the inclinometer and found that the inclinometer had been moved and was not attached propperly to the CART. Evaluated situation." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke circulation and increased rate to 1500 lpm 4.2 bars. Total pumped 50m³ sea water, hook load 109 MT. Closed the IBOP had 25 bars back pressure." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Mixed and pumped 53.7 m³ 1.52 sg Tuned Light XL cement slurry at 1100 lpm, 22 bars pump pressure. Confirmed returns to seabed. Displaced cement slurry with 6.5 m³ of SW at max rate using cement unit. FCP 5.7bars, 600lpm. Bled off pressure, 250 l. Checked for back-flow." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed cmt hose and flushed through manifolds and hoses." "On 2007-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Waited for cement to set. Meanwhile serviced aft PRS. Repaired the auxiliary pump. Serviced the ROV." "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Continued waiting for cement to set. Meanwhile serviced AFT PRS. Repaired the auxiliary pump. Serviced the ROV." "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to release the CART." "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Took digiquartz readings. Confirmed that conductor had not moved." "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued waiting for cement to set." "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Waited for cement to set. Meanwhile work on encode for aft PRS" "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 221m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Took digiquartz readings. F-7 96128mm - F-15 96172mm = F-15 44mm deeper. Slacked of weight to 79MT F-15 94mm deeper then F-7." "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Released CART tool. Broke out and laid out the side entry sub. Racked back one stand with two 2 5½' pups. Dropped one sponge ball and flushed landing string and inner string with sea water. Continued pull out with landing string. With CART in rotary removed 2' valve handle and inclinometer. Function tested CART." "On 2007-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke out X/O and racked back the CART tool in derrick. Laid out the aluminium inner string. Terminated drilling operation due to manning up for dedicated work in processing module." "On 2007-12-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Held tool box talk prior to skid cantilever." "On 2007-12-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Skidded cantilever from F-5 to F-15" "On 2007-12-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Cleaned and cleared rig floor. Prepared for changing out the wash pipe." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Changed out the wash pipe. Pressure tested same to 207 bars 5 min." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Changed out bolts in TDS guard." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Removed hatch on well head deck." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box prior to lay out 5½' HWDP and pick up new 5½' HWDP." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Laid out two stands of 5½' HWDP in singels." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Picked up singles of new 5½' HWDP and made up two stands in derrick." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up and make up 26' drilling BHA." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 161m. The activity was categorized as 'drilling -- trip' and lasted for 7.8 hours. Operational details: Removed master bushing and ran 26' Bit / gMWD assy through rotary. Inserted gMWD probe in BHA as per Scientific instructions. Picked up and made up MWD/UBHO assy. Orientated UBHO sleeve as per Scientific instructions. Ran in with BHA, had assistantce from ROV when entering 30' conductor." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 161m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 161m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Inspected and serviced TDS and FWD PRS. Meanwhile held tool box talk prior to start drilling out the 30' shoe track." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 175m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued to RIH with 26' drilling BHA from 161 m to 175 m, installed PS-21 slips." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Made up TDS, washed and reamed from 175 m, tagged cement at 217.7 m. Drilled out 30' shoe track and cleaned out rat hole, using sea water and 20 m3 Hi-vis pills. Drilled new formation from 226m to 241 m. Drilling parameters : Flow 3200 lpm / SPP 74bar / String RPM 0 / Bit RPM 120./ Torque 1 kNm / WOB 1-3 MT." "On 2007-12-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 26' section from 241 m to 350 m MD. Drilling parameters : Flow 4000 lpm / SPP 75-115 bar / WOB 5-10 MT / Torque 1-14 kNm / String RPM 40 / Bit RPM 160. ROP 13-85 m/hr. Average ROP 22 m/hr. Pumped 10 m3 hi-vis sweep for every single drilled. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. Sliding from 241 m to 255 m" "On 2007-12-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 525m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 26' section from 350 m to 525 m MD. Drilling parameters : Flow 4000 lpm / SPP 112-116 bar / WOB 4-8 MT / Torque 1-10kNm / String RPM 40 / Bit RPM 160. ROP 26-46 m/hr. Average ROP 29 m/hr. Pumped 10 m3 hi-vis sweep for every single drilled. Used sling and tugger on centralizer deck on drillpipe to stabilize same before taking survey. At 500m stopped using slings prior to take survey. Sliding from 349 m to 378 m 398 m to 407 m 438 m to 447 m Parallel activity: Tested drilling BOP. Removed wire line unit from rig floor as good MWD survey." "On 2007-12-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 877m. The activity was categorized as 'drilling -- drill' and lasted for 14.5 hours. Operational details: Drilled 26' section from 525 m to 877 m MD. Drilling parameters : Flow 4000 lpm / SPP 117-125 bar / WOB 2-13 MT / Torque 6-14 kNm / String RPM 40 / Bit RPM 160. ROP 16-60 m/hr. Average ROP 24 m/hr. Pumped 10 m3 hi-vis sweep for every single drilled. Sliding from 726 m to 737 m 767 m to 777 m 801 m to 811 m" "On 2007-12-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 877m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: At 877m. Pumped 10 m³ Hi-vis pill & Circulated 1xBU prior to drill into the Utsira Fm. Flow 4500 lpm / SPP 120 bar, reciprocated the pipe when circulated." "On 2007-12-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 889m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled hard stringer from 877 m to 889 m. Flow 3500 lpm / SPP 98 bar / WOB 8-10 MT / Torque 2 kNm / String RPM 0 / Bit RPM 120. ROP 6-8 m/hr. Average ROP 7 m/hr. Pumped 10 m3 hi-vis sweep. Top Utsira 889 mMD / 881.8 mTVD Sliding from 845 m to 854 m 882 m to 889 m" "On 2007-12-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 922m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 26' section from 889 m to 922 MD. Drilling parameters : Flow 3500 lpm / SPP 98 bar / WOB 10 MT / Torque 10-15kNm / String RPM 40 / Bit RPM 145. ROP 4-50 m/hr. Average ROP 44 m/hr. Pumped 15 m3 hi-vis sweep for every single drilled. Sliding from 889 m to 894 m" "On 2007-12-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1079m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Drilled 26' section from 922 m to 1079 m MD. Drilling parameters : Flow 3500 lpm / SPP 90-100 bar / WOB 1-8 MT / Torque 8-18kNm / String RPM 40 / Bit RPM 145. ROP 26-150 m/hr. Average ROP 45 m/hr. Pumped 15 m3 hi-vis sweep for every single drilled. Base Utsira 1079 mMD / 1064.9 mTVD Sliding from 937 m to 1003 m" "On 2007-12-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1079m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Due to high torque when reaming from 1079 m 1070 m. Flow 4000 lpm / SPP 120-130 bars." "On 2007-12-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1095m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 26' section from 1079 m to 1095 m MD. Drilling parameters : Flow 4000-4500 lpm / SPP 90-100 bar / WOB 6-8 MT / Torque 1-3 kNm / String RPM 40 / Bit RPM 145. ROP 2-15 m/hr. Average ROP 10 m/hr. Pumped 10 m³ hi-vis sweep for every single drilled. Sliding from 1080 m to 1095 m" "On 2007-12-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1333m. The activity was categorized as 'drilling -- drill' and lasted for 14.0 hours. Operational details: Drilled 26' section from 1095 m to 1333 m MD. Drilling parameters : Flow 3500-4000 lpm / SPP 105-138 bar / WOB 6-11 MT / Torque 7-16 kNm / String RPM 40 / Bit RPM 145-160. ROP 2-130 m/hr. Average ROP 10 m/hr. Pumped 10 m³ hi-vis sweep for every single drilled. Top Skade 1227 mMD / 1209 mTVD Base Skade 1322 mMD / 1296.3 mTVD Slided from 1124 m to 1141 m 1164 m to 1178 m 1204 m to 1218 m 1245 m to 1265 m 1285 m to 1305 m" "On 2007-12-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1333m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Mud pump #1 and #2 shot down. Stopped drilling. Circulated with mud pump # 3, 2000lpm reciprocated the string." "On 2007-12-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1369m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Continued drilling 26' section from 1333 m to 1369 m MD. Drilling parameters : Flow 4000 lpm / SPP 138 bar / WOB 9-12 MT / Torque 7-14 kNm / String RPM 40 / Bit RPM 120-160. ROP 10-15 m/hr. Average ROP 13 m/hr. Pumped 15 m³ hi-vis sweep. Slided from 1133 m to 1145 m" "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued drilling 26' section from 1369 m to 1378 m MD. Drilling parameters : Flow 4000 lpm / SPP 140 bar / WOB 6-9 MT / Torque 8-16 kNm / String RPM 40 / Bit RPM 160. ROP 15-23 m/hr. Average ROP 18 m/hr. Pumped 15 m³ hi-vis sweep." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Circulated hole clean pumped 30 m³ Hi-vis followed by 30 m³ sea water and then 30 m³ Hi-vis. Flow 3500-5000 lpm/ 130 bars Torque 6-9 kNm / String RPM 40 / Bit RPM 190. Reciprocated the string." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Took survey at TD 1378 m. Torque and drag at 1365 m / 200 lpm / 40 RPM / 7-10 kNm / up/down weight 150/130 MT." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Displaced open hole to 1.40 sg mud. Flow 4000-5000 lpm/ 135-260 bars Torque 6-8 kNm / String RPM 40 / Bit RPM 160-190. Reciprocated the string Drag at 1365 m / 200 lpm / up/down weight 150/130 MT." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1365m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Prepared for POOH with 26' drilling BHA. Lined up mud bucket." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1299m. The activity was categorized as 'drilling -- ream' and lasted for 4.0 hours. Operational details: POOH from 1365 m to 1306 m. Took weight, worked string without progress. Reamed out from 1306 m to 1299 m without pumping. Attempted to lubricate out with 1.40 SG mud 300 lpm." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 880m. The activity was categorized as 'drilling -- trip' and lasted for 8.0 hours. Operational details: RIH to 1320 m. Displaced hole to Sea Water at 4200 lpm 141 bars. Backed reamed out from 1320 m to 880 m top Utsira. At 4200 lpm / 135 bars / Torque 14 - 40 kNm." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 880m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Circulated BTM at top Utsira 880 m, 4200 lpm 127 bars." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1168m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: RIH with 26' drilling BHA. Took weight at 1168 m." "On 2007-12-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1205m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: Reamed stand. Slided and rotated stand through obstructions at 1168 m, 1173 m and from 1198 m to 1205 m. Flow 3000 lpm / SPP 80 bars / Torque 7-13 kNm. (connection At 1205 m). Made up new connection." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: Reamed from 1205 m to 1378 m. Flow 4200 lpm / SPP 150 bars / Torque 7-22 kNm/ RPM 40 /Bit RPM 160." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1377m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 30 m³ Hi-vis started displacing out same with 3500 lpm / 108 bars, reciprocated the string." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Displaced 30 m³ Hi-vis around at 5000 lpm / 190 bars. Reciprocated the string." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pumped 100 m³ 1.40 SG mud, 4000 lpm / 125 bars." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- trip' and lasted for 5.2 hours. Operational details: Lubricated out of hole with 26' drilling BHA, from 1378 m to 798 m, flow 1000 lpm / SPP 3 bars / RPM 40 / bit RPM 70, torque 6 - 8 kNm." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 798m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: At 798 m displaced well to 1.40 SG mud, flow 4000 lpm / SPP 150 bars. Reciprocated the string. Pumped a total of 475 m³ 1.40 SG mud since started lubricating out of the hole." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 238m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH with 26' drilling BHA from 798 m to 238 m. Worked through tight spot at 548 m. Overpull 15 - 20 tonnes." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Continued POOH with 26' drilling BHA from 238 m to 156 m." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 156m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Made up string to TDS. Topped up the hole with 15 m³ 1.40 SG mud. Meanwhile cleaned rig floor." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 121m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Pulled bit out of funnel 121 m. Held tool box talk prior to change out PS-21slips to master bushing and check dies on PRS. Performed same." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.8 hours. Operational details: Continued POOH with 26' drilling BHA from 121 m. Removed clay as BHA were pulled out. Stabiliser above bit was covered in dry clay. Racked back 8¼' DC. Laid out NMDC, MWD and Motor." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor. Held tool box talk prior to rig up 20' casing handling equipment." "On 2007-12-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Started to rig 20' casing handling equipment." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Continued rigging up 20' casing handling equipment, Odfjell casing tong and FAC tool. Changed to 20' bails and elevator. Installed PS-30 slips." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Crew change, handover between day/night shift." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued rigging up 20' casing handling equipment." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to run 20' casing." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up shoe joint and made up intermediate joint, Baker locked same. Filled shoe with SW for integrity test." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 20' casing from 36 m to 138 m. Filled every jnt with SW." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 214m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Entered 30' conductor at 138 m continued RIH with 20 casing to 214 m. Filled every jnt with SW. Hydraulic hose came off elevator." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 214m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Re-connected hydraulic hose to elevator." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 448m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Continued RIH with 20' casing from 214 m to 448 m. Damaged box of jnt # 77. Filled every jnt with SW." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 448m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Laid out jnt # 77." "On 2007-12-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 956m. The activity was categorized as 'drilling -- casing' and lasted for 7.8 hours. Operational details: Continued RIH with 20' casing from 448 m to 956 m. Filled every jnt with SW." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1052m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued RIH with 20' casing from 956 m to 1052 m. Took 5 MT weight at 1052 m . Filled every jnt with SW." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1055m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Engaged FAC tool. Had to use PRS to align FAC tool due to strong sea current. Established circulation of 220 lpm / 28 bars. Washed down from 1052 m to 1055 m." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1155m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued RIH with 20' casing from 1055 m to 1155m. Unable to get good shoulder indication on graf as making up jnt # 18 and 19. Filled every jnt with SW." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1144m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Laid out jnt # 18 and 19" "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 20' casing from 1144 m to 1218 m. Filled every jnt with SW. Up/down weight 222/184 MT." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held tool box talk prior to change over to 5½' handling equipment. Performed same." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up and install 18 3/4' WH with CART. Unable to open/close 5½' elevators." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Trouble shooted elevator. Rigged down 5½' elevator. Changed out hydraulic filter." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Trouble shooting failure on elevator. Meanwhile rigged up 20' casing elevator. Attempted to move string with 28 MT overpull (250 MT on weight indicator)." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Held tool box talk prior to install 20' circ. swage and cmt. hose. Performed same." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Picked up 20' casing. Had to pull 128 MT overpull to free casing (350 MT on weight indicator). After casing freed up/down weight 230/190 MT. Rigged down 20' casing elevator. Rigged up 5½' DP elevator. Rigged down 20' circ. swage and cmt. hose." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and made up 18 3/4' WH with CART." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Removed PS-30 slips and installed master bushing." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1218m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared rig floor. Rigged down casing tong." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Continued RIH with 20' casing from 1218 m to 1362 m. Washed down from 1294 m to 1362 m with 500/1000 lpm / 37 bars due to increasing holedrag. Returns observed through cementing ports in F-5 conductor." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to pick up and make up CMT head. Performed same." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Established circulation, 500 lpm / 32 bars. Up/down weight 245/187 MT. Landed 18 3/4' WH into 30' conductor by setting down casing string weight plus 5 MT of landing string weight and engaged lock ring. Performed pull test to 25 MT over total casing and landing string weight." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Kept landing string in tension with an overpull of 3 MT while circulating. Establish circulation carefully in steps with SW through top drive to 2300 lpm 23 bars. Observed returns from F-5. ROV surfaced and picked up 4 conductor plugs, dived and installed conductor plug after having pumped 166 m³ of SW. Circulated 1 x casing volume ( 220 m³). Returns up F-15. Pressure tested the cement line to 200 bars 10 mins. Meanwhile held tool box talk prior to perform cement operation of 20' casing." "On 2007-12-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Commenced cementing Lead slurry, 1.52 SG of 20' casing, 1300 lpm 32 bars. Released preloaded ball (1 3/4') for bottom wiper plug." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Mixed and performed cmt job. Pumped : 322 m³ 1.52 SG lead slurry at 1300 lpm, 25 - 28 bars pump pressure. 20 m³ 1.92 SG tail slurry at 900 lpm, 25 bars pump pressure. Good returns in F-15" "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Released dart, shear pressure/volume 200 bar/1250 litres. Chased dart with 3000 litres SW with CMT pump. Displaced cement with rig pumps at 3000 LPM. FCP 52 bars. All returns up F15. Bumped plug at 9507 stks. Increased pressure to 120 bars. 97.6 % pump efficiency." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Bled off pressure = 1500 litres, no back flow." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rigged down CMT hose and control lines." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to release the CART tool." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 145m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Reduced over pull on landing string to neutral. Released CART according to Vetco procedure, 5 turns right hand. Broke out cement head and laid out same. Dropped 2 sponge balls and flushed landing string." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 125m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Laid out two HWDP. Picked up CMT head and broke out 6' DP pup. Laid out CMT head." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued pull out with landing string and laid out same." "On 2007-12-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.0 hours. Operational details: Installed well head hatches. Terminated operation on F-15" "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Held tool box talk prior to skidding of cantilever from F-9 to F-15." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Removed final scaffolding. Skidded cantilever 1.5 m STB. - 2.25 m. AFT, from F-9 to F-15." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pull Master bushing and install HPDR Spider." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed slings in elevator to pull in HPDR Spider. Installed back-up tugger wire." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled Master bushing and installed HPDR Spider. 14:45 Informed production to shut in well Oil producer F-14." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Rigged up to run HPDR Riser and removed hatches. Installed Cradle and trolly on HTS. Parallel activity: Installed VX ring in sub sea well head." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk prior to pick up TBC/HPDR double A." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up TBC/HPDR double A, Meanwhile installed guide wires through slot F 15. 17:50 Oil producer F-14 shut in." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk and check equipment." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Ran tugger to moon pool. Picked up hot stab and attached to TBC. Pressure tested primary lock, primary unlock and secondary unlock. 3000psi(207 bars)/5 mins. Meanwhile rigged up to run guide lines." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed hot stab. Removed hatches and secured open areas. Shut in water injection wells F-4 and F-5." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 1.5 hours. Operational details: Waited for production to bleed off pressure in water injector F-4 and F-5 flow lines." "On 2008-09-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran in with TBC/HPDR double A, landed of TBC/HPDR double A in spider." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.2 hours. Operational details: Picked up double B simultaneous lift by deck crane and the TDS. Removed the riser lifting tool from TBC/HPDR double A. Made up the HPDR double B, Leak tested the connection to 3000 psi(207bars)/10 mins. Installed bolt caps and fairings." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 51m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lowered the HPDR double B. Installed guide wire lines. Hung off HPDR in the riser spider." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Picked up double C simultaneous lift by deck crane and the TDS. Removed the riser lifting tool from TBC/double B. Made up the HPDR double C, Leak tested the connection to 3000 psi(207bars)/10 mins. Installed bolt caps and fairings." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- wait' and lasted for 0.2 hours. Operational details: Entered the water splash zone. To much movement, pulled HPDR out of the water." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- wait' and lasted for 2.8 hours. Operational details: Waited for sea to calm down to be able to run in with HPDR." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lowered the HPDR double C. Hung off the HPDR in the spider." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Picked up double D simultaneous lift by deck crane and the TDS. Removed the riser lifting tool from double C. Made up the HPDR double D, Leak tested the connection to 3000 psi(207bars)/10 mins. Installed bolt caps and fairings. Parallel activity: Prepared equipment for installation of boat collision stool and tension cylinders. Completed BOP testing to 15.000 psi. Derrick inspection. F-9 handed over to production at 13:30" "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lowered the HPDR double D. Observed TBC/HPDR with ROV. Hung off the HPDR in the spider." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Picked up Tension/BOP jnt and Claxton NT-2 RT simultaneous lift by deck crane and the TDS. Removed the riser lifting tool from double D. Made up the Tension/BOP jnt and Claxton NT-2 RT. Leak tested the connection to 3000 psi(207bars)/10 mins." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Held tool box talk, cleared and cleaned rig floor, packed Bandak HPDR make up tools and removed the HPDR spider slips." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 129m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lowed the HPDR string so the Claxton NT-2 RT just below rotary. Installed the master bushing. Hung of in slips and made up one 5½' std. Removed the hole cover from RLGF." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Ran in with the TBC/HPDR. Entered the RLGF. Removed the RLGF, confirmed hot stab orientated for ROV." "On 2008-09-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Landed TBC/HPDR on wellhead and set down 15 MT. Verified TBC fully landed by observing marker/band on TBC. Locked TBC connector. Observed upwards movement on TBC upper body as locking TBC held pressure 3000psi/5 min." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Applied 15 MT overpull and confirmed TBC locked. Removed hot stab and installed dummy hot stab. Slacked off and maintain 10 MT overpull on riser. Informed production to start up Water injector F-4, F-5 and Oil pruducer F-14 at 00:30. Parallel activity: Prepared equipment for Claxton NT2 RT removal and horizontal tensioning systen installation." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed 6 MT tugger from template riser guide." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Began installation of hatches on weather deck." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Waited on production to start up Water injector F-4, F-5 and Oil pruducer F-14. Meanwhile filled HPDR with water in preparation for testing. Pulled 10 MT tugger from guide funnel to surface." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Continued to installation of hatch covers on weather deck." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed horizontal tension system." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Started building scaffolding around Claxton NT2 connector" "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: Built scaffolding around Claxton NT2 connector. Parallel activity: Prepared for installation of Boat collation stool and tension cylinders. Prepared tools to disconnect the Claxton tool. Prepared 17½' BHA Pressure tested standpipe and kill manifold 345 bars." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Filled riser prior to leak test TBC/HPDR/20' CSG/Shoe." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Attempted to leak test the TBC/HPDR/20' CSG/Shoe 20/195 bars 5/10 mins. Pressure drop 2.5 bars/5 mins." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Rigged up to leak test through kill out let in the Moon Pool 15k hose." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Leak tested surface lines, kill out let in the Moon Pool 15k hose. 20/200 bars 5/10 min." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Attempted to leak test the TBC/HPDR/20' CSG/Shoe 20/195 bars 5/10 mins. Pressure drop 2.5 bars/5 mins." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Rigged down 15k test hose from Claxton tool. Prepared for building scaffolding around NT2 connector." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RU Boat collision stool and tension cylinders." "On 2008-09-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.8 hours. Operational details: Started installation of the Boat collision stool and tension cylinders. Parallel activity: Built scaffolding around NT2 connecter." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.5 hours. Operational details: Continued installation of boat collision stool and tension cylinders. Parallel activity: Removed mandrel from BOP, hose and lo-torq from Claxton running tool. Pressure tested kill, cement and choke manifolds to 20/345 bars 5/10 mins." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Applied 50 bars to all tension cylinders. Slacked off TDS weight to natural weight. Increased pressure to 90 bars to the tension cylinders. Measured vertical distance from underside of tensioner ring to upper surface of Boat Collision stool 530mm." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared for rigging down Claxton tool." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held tool box talk and rigged down Claxton tool. Parallel activity: Leak tested Choke manifold 20/345 bars 5/10 mins." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Retrieved Claxton tool and laid out same." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Started nippling up drilling BOP. Parallel activity: Performed maintenance of elevator. Pressure tested TDS 20/1000 bars 5/10 mins. Pressure tested Kelly hose 20/345 bars 5/10 mins." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Installed tension cylinders on the BOP. Parallel activity: Rigged up for running the Slick jnt." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Attempted to install Diverter. BOP/HPDR not align." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Lifted Diverter. Disconnected BOP from HPDR and aligned BOP over well centre below Diverter." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Tool box talk and checked equipment." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Orientated HPDR using the horizontal tension system." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Made up BOP NT2 connector" "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box talk and made up Slick jnt to Annular BOP." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Orientated and landed the Diverter." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed Diverter RT. Connected overshot packer hose. Took BOP weight with upper tension cylinders. Rigged down slings from bails." "On 2008-09-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Tool box talk prior to pick up WBBRT and jetting sub." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed and checked 5½' handling equipment." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up and made up WBBRT and jetting sub. RIH to 139m" "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Jet washed the well head with 4700 lpm 57 bars reciprocated the string." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Ran in, latched on to Nominal Seat protector and retrieved same. Pulled back up to 139m." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Jet washed the well head with 4700 lpm 57 bars reciprocated the string." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH with Nominal Seat protector and jet sub. Laid out Nominal Seat protector and jet sub." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Picked up and ran in with BOP test plug and jet sub. Installed BOP test plug at 141,7m" "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Function tested two set of BOP Rams." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Leak tested kill from cmt unit to BOP 100/345 bars 5/10 mins." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.2 hours. Operational details: Started pressure test of BOP/HPDR against BOP test plug and closed pipe rams. 20 bars 5 mins. Increased pressure to 345 bars." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Pressure tested BOP/HPDR against BOP test plug and closed pipe rams. 345 bars 10 mins. Pressure drop 0.8 bars over 10 mins. Fluid pumped 500 litres, return 500 litres." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: POOH with BOP plug and jet sub. Laid out same. Parallel activity: OOH with BOP plug and jet sub. Closed BOP shear rams and leak tested BOP/HPDR/20' CSG/Shoe to 75 bars. Pressure dropped 1.6 bars over 10 mins." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Made up wear bushing, RIH and installed wear bushing at 140.4 m" "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH with wear bushing RT and laid out same." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor. Checked equipment." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 127m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Held tool box talk, Picked up and RIH with 17½' drilling BHA, from surface to 127m." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 127m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Installed auto slips. Functioned auto slips and found hydraulic leak." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 127m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Repaired hydraulic leak in auto slips." "On 2008-09-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 695m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued RIH with 17½' drilling BHA on 5½' DP from 127m to 695m. The top 5½' DP jnt was bent when hit by TDS. Area was barried off. No dropped object. ***Operations transferred to F-99***" "On 2008-09-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 695m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held toolbox talk before continuing tripping after repairs." "On 2008-09-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 854m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 695 m to 854 m MD. Experienced problems with PRS and racking system." "On 2008-09-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 854m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: troubleshot fwd PRS and racking system." "On 2008-09-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1055m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 17 1/2' BHA on 5 1/2' DP from 854 m to 1055 m MD." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1300m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 17 1/2' BAH on 5 1/2' DP from 1055 m to 1300 m MD." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1300m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held toolbox talk." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1338m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Made up TDS to DP. Filled DP with seawater. Took up/down weights 132/115 MT. Washed down to 1337 m MD. Pumprate 2000 lpm / 30 rpm / Torque ~8 k Nm. No obstruction encountered." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1339m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Picked up and made up 6 m pup for drilling shoetrack. Continued washing down with same parameters and tagged landing collar at 1339 m MD." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped 5 m3 LCM + 1m3 sacrificial spacer at ~1500 lpm. Chased LCM pill with 830 strokes seawater pumping at 2000 lpm / SPP 17 bar. Pulled pipe back to 1307 m MD at controlled speed when LCM entered well." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up cement unit to pump down pipe and kill line on BOP. Performed line test against standpipe isolation valve and HCR on BOP - 100 bar / 10 min - ok. Closed UPR." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Started pressuring up at well. Pumped a total of 1000 lpm before any pressure build up could be seen, probably caused by drained standpipe. Reset volume counter at 5 bar. Pressured up to 75 bar pumping at 100 lpm. Held pressure for 20 min, observed pressure drop of ~1,6 bar / 10 min and ~1,4 bar / 10 min towards end. Hard to determine if leakage rate was improving. Pressured up to 75 bar again. Held test for another 20 min, observed pressure drop of 1,3 bar / 10 min towards end of test, but hard to see further improvement. Estimated leakage rate approx 1,5 l/min. Volume pumped and bled back 943/910 liters. Decided to continue operations." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1339m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed choke drill." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1339m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Established parameters for drilling float collar / shoe track. Flow 3500 lpm / SPP 71 bar / 60 rpm." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Drilled float collar/shoetrack from 1339 m to 1355 m MD. Parameters : Flow 3600 lpm / SPP 73 bar / 70 rpm / WOB 8 MT / Torque 6-20 kNm." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 5 m3 LCM pill and displaced same with 18 m3 stroke at 2000 lpm" "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Lined up cement unit to pump down pipe and BOP kill line. Pressure tested 20' casing to 75 bar. Observed approx 1 % drop last 10 min of test. Attempted to resume drilling shoetrack, got problems with VICIS system / drilling controls." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1355m. The activity was categorized as 'interruption -- other' and lasted for 6.2 hours. Operational details: Circulated on well while working on problem with VICIS." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Established drilling parameters : Flow 3600 lpm / 70 rpm / 10 kNm / 75 bar SPP." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Drilled 20' shoetrack from 1355 m to 1368 m MD. Drilling parameters : Flow 3600 lpm / SPP 75 bar / 70 rpm / WOB 5-6 MT / Torque 10-12 kNm. Pumped 10 m3 hi-vis pills according to program." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleaned rathole from 1368 m to 1378 m MD. Drilling parameters : Flow 3600 lpm / SPP 75 bar / 70 rpm / WOB <1 MT / Torque 10-12 kNm. Reamed back in shoe for every 2 m cleaned. Pumped 10 m3 hi-vis pills according to program." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1381m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled 3 m new formation from 1378 m to 1381 m MD. Drilling parameters : Flow 3600 lpm / SPP 75 bar / 70 rpm / WOB 5 MT / Torque 11 kNm." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1338m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Pumped 20 m3 hi-vis to clean hole. Circulated 1,5 times bottoms up at 3600 lpm / SPP 80 bar to clean the hole." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1338m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pumped 9 m3 LCM pill at 2000 lpm. Chased LCM with 26 m3 seawater. Found that diplacement/spotting of pill was wrong and that the pill had been overdisplaced/dilluted with approx 8 m3 seawater. Discussed situation. Decided to circulate out LCM pill and mix new LCM." "On 2008-09-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Displaced out LCM pill with seawater at 3600 lpm." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Displaced out pill with seawater. Meanwhile started mixing new LCM pill." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Mixed LCM pill. Had problems with plugged auger screw in dry additive system. Added calcarb and steelseal by manual means. Meanwhile circulated hole at 2000 lpm inside 20' casing." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1338m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 9 m3 LCM at 2000 lpm. Chased LCM with 19 m3 seawater. POOH from 1381 to 1338 m MD when spotting the last 4 m3 of LCM. After shutting down pumps, experienced up to 30 MT overpull in interval 1360 to 1350 m MD. Came free to normal weight around 1350 m MD. Pulled back to 1338 m MD." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1338m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: Lined up cement unit and verified line up down drillstring and in kill line on BOP. Perfomed line test to 100 bar / 5 min - ok. Closed BOP. Filled system with 1,8 m3 seawater - zeroed volume counter at 5 bar. Performed fit to 1,50 EMW by pressurising up on well to 64 bar at 100 lpm. Held FIT for 10 min - 1,6 bar leak off. Volume pumped and bled back 972/910 liter. ***Operations transferred to F-15S***" "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1338m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flowchecked well - well static. Held toolbox talk prior to displacing well to OBM." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1381m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH from 1338 m to 1380 m MD with 17 1/2' BHA. Started pumping 1,44 sg OBM. Stepped up rate in increments to 3400 lpm / SPP 75 bar - verified returns. Rotated at 30 rpm / torque ~12 k Nm. After approx 34 m3 pumped observed pack off tendencies with SPP peaking rapidly to 180 bar. Stopped pumping. Trapped pressure on standpipe 32 bar. Bled off standpipe pressure." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1381m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Attempted to work string free. Not able to come down - string at TD. Attempted to come up - functioned jar twice. Attempted to work string free by applying torque up to 40 kNm and overpull of 40 MT. Made way from 1381 m to 1376 m MD. Attempted to pump - hole still packed off. Bled off 27 bar pressure trapped on standpipe and heard loud roarring sound. Lost string weight - went to just above block weight. POOH with 5 1/2' DP and found string screwed out underneath 6 m drilling pup joint. Laid out pup joint - found no damage on threads." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.8 hours. Operational details: Discussed fishing alternatives and way forward." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Held pre-job meeting for attempting to screw into drillpipe." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 42m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: 1RIH with 5 1/2' DP. Tagged fish at 41,6 m MD indicating that drillstring had fallen to the bottom of the well." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 42m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: Attempted to screw into DP coupling at 41,6 m MD - negative. Meanwhile traced fishing equipment." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 42m. The activity was categorized as 'interruption -- fish' and lasted for 1.2 hours. Operational details: Removed auto slips from rotary. Pulled DP to different positions relative to wellcenter in attempt to enter threads in drillstring. Entered DP thread successfully. Meanwhile traced fishing equipment." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1380m. The activity was categorized as 'interruption -- fish' and lasted for 0.2 hours. Operational details: Made up DP coupling at 41,6 m MD with topdrive. Increased torque in increments of 5 kNm to a total of 45 kNm. String broke free at 45 kNm." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1380m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Installed auto slips in rotary." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1380m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Picked up string weight ~120 MT. Observed pipe free to move in intervall 1381 to 1372 m MD without applying overpull. Rotated string with 10 rpm / ~10 kNm." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1372m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Made plans for regaining circulation and continue displacement to OBM. Made plans for routing contaminated returns back to pits. Meanwhile rotated string with 10 rpm / ~10 kNm." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1372m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Started filling string which was partly empty due to u-tubing. Verified returns. Stepped up rate to 1500 lpm / SPP 5 bar. Routed returns back to pits." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1372m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Caught up with u-tube after pumping approx 60 m3. Stepped up circulation rate in increments to 2900 lpm / SPP 105 bar. Total volume of OBM pumped 253 m3." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' drilling BHA from 1372 m to 1357 m MD. Experienced 5-6 MT overpull when pulling bit through shoe at 1368 m MD. Experienced 12-15 MT overpull at 1357 m MD, depth corresponding to casing coupling between shoe joint and intermedate joint relative to near bit stab in BHA." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Made up TDS. Broke circulation and stepped up rate in increments to 2000 lpm / SPP 55 bar. Made several attempts to pass restriction with and without rotation - negative." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1357m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Set torque limit to 25 kNm. Set rotation at 15 rpm and worked restriction with ~5MT overpull. Observed increasing torque fluctuating between 7 and 25 kNm." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Came through restriction at 1357 m MD. Worked new restriction at 1355 m with overpull and broke through. POOH to 1337 m MD." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1337m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Broke, inspected and racked back stand used for fishing drillstring." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1337m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Flowchecked well - static. Rebooted VICIS system due to problems with ZMS." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1329m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Inspected threads on DP coupling in RT- found some damage / scoring. POOH with DP single to 1329 m MD. Observed gain in triptank indicating swabbing when pulling single. Flowchecked - well static. Broke out single and laid out. Picked up new DP single and made up to stand." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made up TDS. Emptied triptanks. POOH with 17 1/2' BHA from 1329 m to 1297 m MD while pumping at 1500 lpm / SPP 26 bar. Prevailing problems with ZMS / VICIS / control system." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot ZMS / VICIS / control system." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Broke and racked back stand. Made up TDS to string for circualting on well due to swabbing and troubleshooting ZMS / VICIS / control system." "On 2008-09-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Broke circulation and stepped up rate to 2500 lpm / SPP 82 bar. Observed sudden drop in pump pressure of 8 bar after pumping for 10 mins. Increased pump rate to 3500 lpm / SPP 131 bar. Observed steady flow of LCM, clays and rubber over shakers. Also found a few small chunks of cement. Meanwhile troubleshot ZMS / VICIS / control system." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Circulated on well at 3500 lpm / SPP 130 bar. Meanwhile troubleshot ZMS / VICIS / control system" "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot ZMS / VICIS / control system. Meanwhile circulated on well 3500 lpm / SPP 130 bar." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Had black out on mainpower due to incident caused by production. Lost power on all drilling systems." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1297m. The activity was categorized as 'interruption -- other' and lasted for 2.8 hours. Operational details: Troubleshot ZMS / VICIS / control system." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1257m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Calibrated travelling block while POOH with stand - still problems with control system / ZMS limits. Racked back stand. Decieded to start POOH with reduced speed." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1117m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 1257 m to 1117 m MD. No swabbing or excessive overpull observed." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 127m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: POOH with 17 1/2 BHA on 5 1/2' DP from 1117 m to 127 m MD. Pulled at reduced speed due to problems with ZMS / control system." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 127m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked before pulling BHA well static. Dropped 2 3/8' drift in HWDP." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 88m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' HWDP from 127 m to 88 m MD." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 88m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Removed PS-21 auto slips from rotary. Inserted masterbushing. Prevailing problems with ZMS / control system. Halted operation for troubleshooting." "On 2008-09-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 88m. The activity was categorized as 'interruption -- other' and lasted for 10.2 hours. Operational details: Troubleshot problems with ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 88m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot problems with ZMS / control system. Got system up and running sufficiently to continue operations. Block/TDS out of ZMS. Discussed compensating measures." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 88m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for handling 17 1/2' BHA." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH with 17 1/2' drilling BHA. Broke out and racked back jar, DC and NMDC. Broke and laid out 17 1/4' stabilizer. Made SJA for handing and tripping with partly functioning ZMS system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Problems with ZMS. Rebooted ZMS system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with NBS and 17 1/2 bit. Inpected bit. Found some worn theeth and chunks of aluminium trapped in the bit. No excessive wear on stabilzers. Drift trapped in BHA." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleaned and tidied drillfloor. Measured distance from RT to bottom of flowline." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for picking up 12 1/4' drilling BHA." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Picked up and hung off 12 1/4' PDX5 in rotary. Picked up and made up Powepulse. Picked up and made up ARC-8." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made up ARC. Secured with dog collar." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Made up NMDC, DC, Jar, drfit sub and 5 1/2' HWDP. Halted operation for work on ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Troubleshot ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk for potential dropped object check. Meanwhile troubleshot ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Checked TDS and PRSs for loose objects (PDO). Meanwhile troubleshot ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Conducted kick drill. Installed TIW. Meanwhile troubleshot ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Troubleshot ZMS / control system. Meanwhile troubleshot ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Troubleshot ZMS / control system. Meanwhile held toolbox talk for rigging 3' chicksan on F-5." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Troubleshot ZMS / control system." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Troubleshot ZMS / control system. Meanwhile rigged 3' chicksan in moonpool." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 212m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Reset all drilling system - got ZMS / control system up and running." "On 2008-09-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Broke and racked back 2 std x HWDP stands, HWDP and jar, 2 std x DC, 1 std NMDC. Meanwhile rigged 3' chicksan in moonpool." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Made up 6 m pup joint on drilling BHA. Powered down batteries in MWD. Racked back 12 1/4' drilling BHA in derrick." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Cleared, cleaned and tidied drillfloor." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Made up nominal seat protector pulling tool. RIH to 139,3 m and latched on to nominal seat protector. Released seat protector with 20 mT overpull." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with nominal seat protector. Broke and laid down pulling tool and nominal seat protector." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up and made up BOP test plug. RIH with test plug to 139 m MD. Spaced out for low stick up during BOP test." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Installed pup joint. Landed BOP plug in wellhead at 140,6 m MD. Retracted block and installed test swadge on TDS." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Lined up cement unit. Performed line test to 345 bar - ok." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 6.5 hours. Operational details: Tested BOP to 20/290 bar 5/10 min - 9 tests in total including IBOP." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Broke out swadge/cement hose from TDS. Not able to move TDS - problems with ZMS / control system." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot ZMS / control system." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH with BOP test plug on 5 1/2' DP from 140 m MD to surface. Broke jet sub and laid out. Broke test plug and laid out." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleared and tidied drillfloor. Observed hydraulic leak on Iron Roughneck" "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired hydraulic leak on Iron Roughneck" "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Picked up nominal seat protector and installed new seals." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RIH with nominal seat protector on 5 1/2' DP from surface to 140 m MD. Set nominal seat protector according to Vetco instructions." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH with nominal seat protector running tool, broke and laid down same. Cleared and tidied drillfloor." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for making up 12 1/4' BHA." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 185m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Hung off 12 1/4' drilling BHA. Removed magnet and downloaded ARC. Made up NMDC, 8 1/4' DCs, jar and 5 1/2' HWDP. Installed PS-21 automatic slips." "On 2008-09-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 297m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 185 m to 297 m MD." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 980m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 297 m to 980 m MD." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 980m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Filled drillstring. Stepped rate up to 2500 lpm. Tested MWD. Adjusted ECD values - ok. Meanwhile tested 3' chiksan line to F-5 - observed minor leaks/drips from line. Hammered up connections in question. No leaks on valve assembly." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 980 m to 1307 m MD. Meanwhile tested 3' chicksan line to F-5 against KWV to 380 bar - 7 bar drop / 10 min (1,86% drop)" "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Prepared for doing slip and cut. Rigged up swadge on drillstring to maintain circulation in well. Stepped up pumps to 2500 lpm as dictated MWD. Meanwhile tested 3' chicksan line to F-5 against closed lo-torque - 2,5 bar / 10 min (0,65%) - ok." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Performed slip and cut of drill line. Problems with deadline anchor." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Had problems with bolts on deadline anchor spooler drum." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Slip and cut drill line." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'interruption -- other' and lasted for 3.8 hours. Operational details: Slip and cut drill line. Had problems with bolts on deadline anchor clamp." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1307m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Broke out swadge on drillstring." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1355m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 1307 m to 1355 m MD. No obstructions observed." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Staged up pumps to 3000 lpm / SPP 129 bar / 30 rpm. Washed down to 1368 m MD - no obstructions seen. Stopped pumping and rotation pulled back to 1353 m - no overpull. Ran back in to 1368 m MD." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Established parameters for washing down / cleaning rathole : Flow 3000 lpm / SPP 128 bar / Rotation 60 rpm / torque 6 kNm. Washed down from 1368 m to 1374 m MD. Observed sudden torque build up followed by pack off - pump pressure peaked at 180 bar. String free to move down. Regained circulation at 3000 lpm / 128 bar SPP. Worked string upwards and pulled into casing shoe at 1368 m MD while circulating at 3000 lpm." "On 2008-09-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Circulated hole clean. Parameters : Flow 3300-4000 lpm / SPP 150-207 bar / 60 rpm / Torque 7 kNm." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1381m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 12 /4' BHA from 1368 m to TD at 1381 m MD. Prameters : Flow 4000 lpm / SPP 204 bar / 60 rpm / torque 6-8 kNm. No obstructions or rapid torque build up seen." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1416m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 12 1/4' hole section from 1381 m MD to 1416 m MD. Parameters : Flow 4000 lpm / SPP 202 bar / 100 rpm / torque 7-9 k Nm / WOB 1-3 MT / ECD 1,43. Downlinked powerdrive according to Schlumberger procedure." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1416m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Observed pack-off tendencies at 1416 m MD. Pressure increased rapidly from 205 to 220 bar. Torque peaked at 25 kNm. Observed 8 m3 losses in active. Worked string and regained circulation. Discussed situation." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1416m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Circulated hole clean at 2600-4000 lpm / SPP 100-203 bar." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 1416 m to 1368 m MD. Pumped at 4000 lpm / SPP 203 bar while pulling. Rotated string 10 rpm. Hung up with 3-4 MT when comming through shoe with bit." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1366m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Circulated hole clean at 1366 m inside 20' csg shoe, 4000 lpm / SPP 193 bar." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1416m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Washed down from 1366 m to 1416 m, 4000 lpm / SPP 193 bar." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1529m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: Drilled 12 1/4' hole section from 1416 m MD to 1529 m MD. Parameters : Flow 4000 lpm / SPP 190-194 bar / 120 rpm / torque 6-15 k Nm / WOB 1-2 MT / ECD 1,45 / ROP 18-25 m/hr. Downlinked powerdrive according to Schlumberger procedure. Meanwhile PU and MU stds of 9 5/8' csg and pressure tested choke mainifold." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1529m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled off btm due to overload on shakers. Circulated 3500 lpm / SPP 195 bar / 80 rpm / torque 6 k Nm." "On 2008-09-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1632m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: Drilled 12 1/4' hole section from 1529 m MD to 1632 m MD. Parameters : Flow 4000 lpm / SPP 195-204 bar / 120 rpm / torque 5-15 k Nm / WOB 2-8 MT / ECD 1,45 / ROP 20-29 m/hr. Downlinked powerdrive according to Schlumberger procedure. Meanwhile PU and MU stds of 9 5/8' csg and pressure tested choke mainifold." "On 2008-09-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1682m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 12 1/4' hole section from 1632 m MD to 1682 m MD. Parameters : Flow 4000 lpm / SPP 208 bar / 120 rpm / torque 8-13 k Nm / WOB 2-5 MT / ECD 1,45 / ROP 20-29 m/hr. Downlinked powerdrive according to Schlumberger procedure. Meanwhile PU and MU stds of 9 5/8' csg." "On 2008-09-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1682m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled off btm due to overload on shakers. Circulated 3330 lpm / SPP 153 bar / 100 rpm / torque 7 k Nm." "On 2008-09-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1723m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' hole section from 1682 m MD to 1723 m MD. Parameters : Flow 4000 lpm / SPP 210 bar / 120 rpm / torque 9-13 k Nm / WOB 2-4 MT / ECD 1,46 / ROP 25-27 m/hr. Downlinked powerdrive according to Schlumberger procedure. Meanwhile PU and MU stds of 9 5/8' csg. A total of 51 std RB in derrick." "On 2008-09-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1738m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' hole section from 1723 m MD to 1738 m MD. Parameters : Flow 4000 lpm / SPP 211 bar / 120 rpm / torque 7-11 k Nm / WOB 3-4 MT / ECD 1,46 / ROP 20-26 m/hr. Downlinked powerdrive according to Schlumberger procedure. Unable to treat cutting within spec. Viscosity too low (below 40 sek). Took cuttings return to skips. Meanwhile PU and MU stds of 9 5/8' csg." "On 2008-09-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1799m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 12 1/4' hole section with limited ROP from 1738 m MD to 1799 m MD. Parameters : Flow 4000 lpm / SPP 211 bar / 120 rpm / torque 7-11 k Nm / WOB 3-4 MT / ECD 1,46 / ROP 10 m/hr. Downlinked powerdrive according to Schlumberger procedure. Unable to treat cutting within spec. Viscosity too low (below 40 sek). Reduced ROP due to lack off cuttings skips. Meanwhile PU and MU stds of 9 5/8' csg." "On 2008-09-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1799m. The activity was categorized as 'interruption -- maintain' and lasted for 6.5 hours. Operational details: Halted drilling due to all cutting skips full. Pulled off btm. Circulated and reamed from 1796 m to 1760 m with 3560 lpm / SPP 171 bar / 80 rpm / torque 7 k Nm while waiting for boat. Attempted to prepare content of slurry holding tank for injection, but were unable to get fluid within viscosity spec. Boat arrived location at 16:15. Transfered content of slurry holding tank to boat from 17:50 to 19:45." "On 2008-09-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1880m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 12 1/4' hole section with limited ROP from 1799 m MD to 1880 m MD. Parameters : Flow 4000 lpm / SPP 215 bar / 120 rpm / torque 8-10 k Nm / WOB 3-5 MT / ECD 1,46 / ROP 10-25 m/hr. Downlinked powerdrive according to Schlumberger procedure. Established new rutines for cuttings treatment and transfer. Meanwhile PU and MU stds of 9 5/8' csg." "On 2008-09-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1998m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole section from 1880 m MD to 1998 m MD. Parameters : Flow 4000 lpm / SPP 222 bar / 120 rpm / torque 11-13 k Nm / WOB 5-9 MT / ECD 1,46 / ROP 3-35 m/hr. Drilled through several stringers. Downlinked powerdrive according to Schlumberger procedure. Meanwhile PU and MU stds of 9 5/8' csg. A total of 63 stds RB in derrick (10 stds with centralizer)." "On 2008-09-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2136m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole section from 2000 m MD to 2136 m MD. Parameters : Flow 4000 lpm / SPP 222-226 bar / 140 rpm / torque 10-13 k Nm / WOB 5-6 MT / ECD 1,47 / ROP 27-30 m/hr. Downlinked powerdrive according to Schlumberger procedure." "On 2008-09-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2133m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: Halted drilling due priority given to frack job in F-5. Pulled off btm. Circulated and reamed from 2133 m to 2083 m with 4000 lpm / SPP 227 bar / 140 rpm / torque 8-12 k Nm." "On 2008-09-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2133m. The activity was categorized as 'drilling -- other' and lasted for 3.2 hours. Operational details: Continued circulating and reaming from 2133 m to 2083 m with 3000 lpm / SPP 136 bar / 80 rpm / torque 9-11 k Nm while waiting for frac job in F-5." "On 2008-09-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2227m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: Drilled 12 1/4' hole section with limited ROP from 2136 m MD to 2227 m MD. Parameters : Flow 4000 lpm / SPP 231-233 bar / 140 rpm / torque 11-17 k Nm / WOB 2-5 MT / ECD 1,47 / ROP 20-25 m/hr. Downlinked powerdrive according to Schlumberger procedure. Reduced ROP due to lack off cuttings skips and the time-consuming job to get content of holding tank within spec and ready for injection." "On 2008-09-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2320m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 12 1/4' hole section with limited ROP from 2227 m MD to 2320 m MD. Parameters : Flow 4000 lpm / SPP 233-237 bar / 140 rpm / torque 12-17 k Nm / WOB 3-4 MT / ECD 1,47 / ROP 18-23 m/hr. Downlinked powerdrive according to Schlumberger procedure. Reduced ROP due to lack off cuttings skips and the time-consuming job to get content of holding tank within spec and ready for injection. 6 skips arrived with boat at 04:00. Performed preflush and prepared for kuttings injection while taking cuttings return to skips." "On 2008-09-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2340m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 12 1/4' hole section with limited ROP from 2320 m MD to 2340 m MD. Parameters : Flow 4000 lpm / SPP 238 bar / 140 rpm / torque 14-15 k Nm / WOB 3-4 MT / ECD 1,47 / ROP 18-23 m/hr. Downlinked powerdrive according to Schlumberger procedure. Reduced ROP while preparing for cuttings injection and taking cuttings return to skips." "On 2008-09-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- drill' and lasted for 10.5 hours. Operational details: Drilled 12 1/4' hole section from 2340 m MD to 2536 m MD. Parameters : Flow 4000 lpm / SPP 239-246 bar / 160-175 rpm / torque 12-22 k Nm / WOB 3-7 MT / ECD 1,48 / ROP 28-31 m/hr. Downlinked powerdrive according to Schlumberger procedure." "On 2008-09-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2536m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: Circulated well clean with 3 x BU while reaming from 2536 m to 2500 m with 4000 lpm / SPP 245 bar / 120 rpm / torque 10-14 k Nm." "On 2008-09-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Pumped a 10 m3 LCM pill at 2000 lpm / SPP 245 bar / 120 rpm / torque 10-14 k Nm and spotted at TD to cover Balder formation. POOH with 12 1/4' BHA on 5 1/2' DP from 2536 m to 2400 m." "On 2008-09-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Dropped and pumped down gyro from surface to 2400 m (bit depth) with 440 lpm / SPP 5 bar." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Continued to pump down gyro from surface to 2400 m (bit depth) with 440 lpm / SPP 5 bar. Landed out in inside 12 1/4' BHA at 2289 m. Established tool faces according to Gyrodata's instructions. Survey taken from 2286.3 to seabed." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well at 2400 m. Static." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2400m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Pumped 4.7 m3 1.70 sg slug at 880 lpm / SPP 17 bar / 10 rpm / torque 7-9 k Nm." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1313m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 2400 m to 1313 m. Pulling speed: 5-6 stds/hr. Performed gyro surveys according to Gyrodata instructions. No obstructions met in 20' csg shoe area." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 186m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: POOH with 12 1/4' BHA on 5 1/2' DP from 1313 m to 186 m. Pulling speed: 7 stds/hr. Performed gyro surveys according to Gyrodata instructions." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: POOH with 12 1/4' BHA from 186 m to OOH. Recovered gyro. LD 2 x monel DC's. Changed to PS 21 and removed master bushings before handling MWD tools and powerdrive. Dumped data from MWD tools and RB in derrick. Cleaned and cleared rig floor." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Held tool box talk for manriding. Serviced and inspected TDS and fwd PRS for loose items. Found cable hanging outside cable tray on PRS dragchain in derrick." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 6.5 hours. Operational details: Man-rode to re-install cables inside PRS drag chain. Made up goose neck for cables to stop them from moving outside drag chain when moving the PRS. Meanwhile performed maintenance and house keeping. Held tool box meeting prior to retrieving nominal seat protector and RU 9 5/8' csg equipment." "On 2008-09-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: PU and MU WBRRT." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Functioned BOP. RIH and jetted BOP at 2000 lpm / SPP 15 bar / torque 10 rpm. RIH with WBRRT and retrieved nominal seat protector at 140.6 m MD. Observed 10 MT overpull to free seat protector. Jetted WH at 2000 lpm / SPP 21 bar. Distance RKB to WH: 138,89 m. POOH with nominal seat protector from 140 m to OOH. LO same. Cleaned and cleared rig floor." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RU 9 5/8' csg handling equipment. RU FAC tool and long bails. Installed FMS. Changed to small wheels on csg tong and installed in front of aft iron roughneck. Recorded steady loss of 100 ltr/hr throughout last 24 hrs." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued RU 9 5/8' csg handling equipment." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Performed pre-job meeting before running csg. PU and MU shoe joint and float joint assemblies. Thread locked connection. Attempted to install bypass baffle in float collar joint." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Bypass baffle was machined down from 9.2' to a proper size to fit inside 9 5/8' csg. Verified and approved from Halliburton onshore that the equipment would work according to plan. Installed bypass baffle in float collar joint." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued to PU and MU float joint and landing collar assemblies. Thread locked connection. Checked integrity of shoe and float when RIH." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 8.2 hours. Operational details: RIH with 9 5/8' csg from 40 m down to 20' csg shoe at 1362 m. Filled every std using FAC tool. Tripping speed: 5-8 std/hr. Experienced problems with Odfjell elevator closing mechanisme. Had to function test and grease it every 6 stds." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1362m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Broke circulation at 20' shoe and circulated with 2000 lpm / SPP 22 bar." "On 2008-09-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1774m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: RIH with 9 5/8' csg from 1362 m to 1774 m. Filled every std using FAC tool. Tripping speed: 4-5 std/hr. Top section of fwd PRS moved forward (along top-most track) until drive section released/broke off and fell over to the side, resting against the upper part of the derrick. Emergency stop was activated. No personnel on drillfloor during the incident. Area was barried off. No dropped objects." "On 2008-10-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1774m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared drillfloor and cantilever off personnel and barried off exposed area if PRS was to fall further. Re-started TDS after emergency stop had been activated." "On 2008-10-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Checked for loose items in derrick. None. Took pictures in derrick and discussed further action. Held meeting regarding the incident. Meanwhile circulated with 650 lpm / 25 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m, due to 20 MT overpull when attempting to reciprocate on full csg std no 16 (1791 m - 1756 m)." "On 2008-10-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Waited for CAN (climbers) to inspect upper part of fwd PRS." "On 2008-10-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Circulated with 1000 lpm / 27 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m. Meanwhile inspected upper part of fwd PRS using climbers from CAN. Removed loose items. Secure lower part of fwd PRS with wire slings to samson post at drillfloor V-door. Secured cable tray and PRS flush joint hanging under upper racking arm with ropes due to high wind forcast." "On 2008-10-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated with 1000 lpm / 27 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m. Waiting for CAN (climbers) to secure upper part of fwd PRS to derrick beam and install net." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Circulated with 1000 lpm / 27 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m. Waiting for CAN (climbers) to secure upper part of fwd PRS to derrick beam and install net. Meanwhile cleaned BOP, installed rubber skirts in wellhead module on F-5 and F-9 and performed general maintenance." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 9.8 hours. Operational details: Circulated with 1000 lpm / 27 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m. Meanwhile CAN (climbers) secured upper part of fwd PRS to derrick beam and inspected PRS for loose items and performed general maintenance." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held time-out-for-safety (tofs) for operation on drillfloor with fwd PRS secured in its current condition." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Performed confidence inspection of PRS and derrick with drill crew." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated with 1000 lpm / 27 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m. Meanwhile layed out and measured 9 5/8' csg on cantilever." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated with 1000 lpm / 27 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m. CAN climbers inspected potential dropped object from PRS beam that had been observed by rig crew. Possible dropped object was found to be a lump of grease." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Circulated with 1000 lpm / 27 bar and reciprocated 9 5/8' csg from 1790 m to 1783 m. Meanwhile continued to lay out and measure 9 5/8' csg on cantilever." "On 2008-10-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Held tool box talk. RD Odfjell elevator and FAC tool. RU laFleur and BX elevator. Installed rollers on HTS. Meanwhile monitored well on trip tank." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1790m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued hooking up and testing of 9 5/8' csg handling equipment. Held tool box talk." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1835m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH with 9 5/8' csg from 1790 m to 1835 m. Filled every 5 joints using laFleur tool. Tripping speed: 2-3 jnts/hr. Nocked off fitting on BX-elevator." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1835m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Replaced and MU new fitting on BX elevator hydraulic hose." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2024m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 9 5/8' csg from 1835 m to 2024 m. Filled every 5 joints using laFleur tool. Tripping speed: 4-5 jnts/hr." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2072m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 9 5/8' csg from 2024 m to 2072 m. Tripping speed: 4 jnts/hr." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2072m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to continue running casing. Meanwhile Westcon inspected PRS for loose items." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2384m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: RIH with 9 5/8' csg from 2072 m to 2384 m. Filled every 5 joints using laFleur tool. Tripping speed: 4-5 jnts/hr." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2384m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.2 hours. Operational details: WOW. Wind speed too high for crane to operate. Could not get casing hanger/PADPRT assy and HWDP landing string. Meanwhile broke circulation at 2384 m. Staged up pumps slowly to 1000 lpm / 30 bar. Reciprocated pipe from 2374 m to 2383 m." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2384m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: LO and measured HWDP landing string. Meanwhile continued to circulate 1000 lpm / 30 bar and reciprocated pipe from 2374 m to 2383 m. Held tool box talk prior to changing handling equipment. Westcon inspected PRS for loose items." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2384m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RD LaFleur circulation tool." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PU and MU casing hanger/PADPRT assy. RIH with casing hanger through rotary." "On 2008-10-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Changed to 5 ½' HWDP handling equipment. Changed from PS30 to PS21 slips. RD and LO csg tong. Cleaned and cleared rig floor." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2519m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH with 9 5/8' csg on 5 ½' HWDP from 2390 m to 2519 m. Sat down 10 MT weight at 2519. RIH with last joint of HWDP. Up weight 185 MT / down weight 132 MT." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2519m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made 5 attempts to pass obstruction at 2519 m without flow. Sat down 15 MT weight each time and on last attempt had 20 MT overpull when pulling out." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2520m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: MU XO and 3 m pup. MU TDS and broke circulation carefully. Increased flowrate in steps of 200 lpm up to 1000 lpm / 20 bar. Washed down and worked csg to pass obstruction at 2519 m. Sat down 15 MT. No increase in pressure was observed. Made several attempts but observed no progress, except for the 20 cm gained on the first attempt. Increased flow to 1400 lpm / 25 bar. Washed down and worked csg to pass obstruction at 2519 m. Sat down 20 MT. No increase in pressure was observed. Made several attempts but observed no progress. Increased flow to 2000 lpm / 40 bar. Washed down and worked csg to pass obstruction at 2519 m. Sat down 30 MT. No increase in pressure was observed. Made several attempts and gained 1m in 15 min." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2522m. The activity was categorized as 'drilling -- casing' and lasted for 9.0 hours. Operational details: Continued to work csg past obstruction at 2520, 2000 lpm / 32 bar. Staged up WOB from 30 MT to 100 MT. No increase in pressure was observed. Gained 2 m." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2403m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: POOH and LO HWDP landing string from 2522 m to 2403 m." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2412m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: WOW. Wind speed too high for crane to operate. Could not lift csg tong onto drill floor or LO hanger/PADPRT assy. Meanwhile MU TDS and broke circulation carefully. Increased flowrate in steps of 200 lpm up to 2000 lpm / 30 bar. Broke out TDS and PU single HWDP to be able to reciprocate without have csg hanger/PADPRT assembly in BOP. Circulated and reciprocated csg from 2412 m to 2406 m, 1000 lpm / 10 bar." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2412m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lifted csg tong onto drill floor. Meanwhile circulated and reciprocated csg from 2412 m to 2406 m, 1000 lpm / 10 bar." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH and LO HWDP from 2412 m to 2393 m." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RU csg tong and changed from PS21 to PS30. Changed to 9 5/8' csg equipment." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH and LO casing hanger/PADPRT assy and 9 5/8' csg joint #310. PU and MU casing hanger/PADPRT assy." "On 2008-10-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RD csg tong. Changed from PS30 to PS21 slips." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2393m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continue to RD csg tong and changed to PS21 slips. Changed to 5 ½' HWDP handling equipment. Cleaned and cleared rig floor." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2515m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 9 5/8' csg on 5 ½' HWDP from 2390 m to 2515 m. Up weight 131 MT / down weight 183 MT." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2515m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PU and MU cmt head. Connected control lines." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Washed 9 5/8' csg down from 2515 m to 2516,7 m with 200 lpm / 7 bar. Landed casing according to Vetco procedure at 140.35 m and sat down 118 MT. PU to 93 MT." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Established circulation with 1.44 OBM in 200 lpm steps up to 2000 lpm. Circulated one btms up volume (220 m3) at 2000 lpm / 40 bar loss free rate. Meanwhile held pre-job meeting for cmt job. Geoservices had black-out on their system." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Geoservices worked to restart their system. Meanwhile continued to circulate at 2000 lpm / 40 bar." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Geoservices worked to restart their system. Meanwhile continued to circulate at 2000 lpm / 40 bar." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Performed hand-over and held pre-job meeting for cmt job. Meanwhile continued to circulate at 2000 lpm / 40 bar." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped 6 m3 base oil and 15 m3 1.55 sg tuned spacer using rig pumps at 2000 lpm / 40 bar. Chased spacer to drill floor with 3 m3 OBM." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Released bottom dart for btm plug. Kept 20 bar back pressure on top drive. Mixed and pumped 13.1 m3 1.90 sg cmt slurry at 800 lpm / 30-50 bar. Btm wiper plug sheared at 180 bar. Displaced cmt to rig floor with 500 ltrs DW. Released top dart and pumped 1500 ltrs DW behind cmt. Top wiper plug sheared at 112.6 bar." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Zeroed stroke counters for mud pumps. Continued displacing cement with 86.8 m3 OBM at 2000 lpm / 40 bar using mud pumps. Wiper plug sheared at 120 bar / 3380 stks. Slowed down rate to 1000 lpm / 16 bar (FCP) approx 4 m3 prior to bump. No bump observed. Stopped after pumping 3980 strokes, theoretical volume + 1/2 shoe track. No losses during displacement. Monitored for back pressure. None observed." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Flushed manifolds and broke off cmt hose to check for back flow." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Set seal assembly according to Vetco procedure. Performed line test of surface line against fail safe valve to 290 bar / 5 min. Ok. 28 ltrs pumped and 28 ltrs bled back. Closed upper pipe ram and lined up TDS to trip tank to monitor for returns. Pressured up in stages to 207 bar below closed ram. Bled off pressure to zero. Opened rams and took 30 MT overpull (110 MT on weight indicator). Closed ram and pressure tested seal assembly 35/290 bar for 5/10 min. Dropped 1.5%. 380 ltrs pumped and 380 ltrs bled back. Reduced overpull to 3 MT. Rotated 4 right-hand turns and released PADPRT." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleaned and cleared rig floor of excess equipment. Held tool box meeting prior to LD cmt head." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2517m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: LD cmt head std. Dropped sponge balls and flushed string with 1000 lpm using OBM." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: POOH with PADPRT from 140 m to OOH. Removed PS21 and installed master bushings. Measured lead impression block to be 1 3/4'. LO PADPRT." "On 2008-10-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held tool box talk before RD handling equipment. Removed elevators and bails. Cleared drill floor of non essential equipment. Monitored well on trip tank. *** Transferred operation to F-5 *** NB! 9 5/8' casing will be tested to 290 bar as parallel activity on F-5" "On 2008-11-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 10.0 hours. Operational details: Transferred operation from F-99 to F-15S. Held tool box meeting prior to pressure testing BOP. Pressure tested BOP to 20/345 bar for 5/10 min. Pressure tested 9 5/8' casing, on 07-10-08 during F-5 well intervention, to 290 bar/15 min. Dropped 2.2 bar (0.8%). 1760 ltrs pumped and 1760 ltrs bled back. Meanwhile installed positioner for PRS FJE." "On 2008-11-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: Pressure tested TDS, upper and lower IBOP and kelly hose to 20/345 bar for 5/10 min." "On 2008-11-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.5 hours. Operational details: RD test equipment. POOH with BOP test tool from 139 m to OOH in singles. Removed PS30 and installed master bushings. LD BOP test tool. Cleared and tidied rig floor." "On 2008-11-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: PU and MU wear bushing assembly. Emptied trip tank. RIH with wear bushing from surface to 30 m. Removed master bushings and installed PS30." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: RIH with wear bushing from 30 m to 139 m in singles." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Sat wear bushing according to Vetco procedure. Made 5 attempts before it was properly installed." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: POOH with wear bushing from 139 m to OOH m in singles. Removed PS30 and installed master bushings. LD WBRRT. Meanwhile pressure tested choke & kill manifolds to 300/15000 psi for 5/10 min." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW for derrick inspection using CAN climbers. Had 35-40 knots wind. Meanwhile started slew calibrating PRS." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: WOW for derrick inspection. Meanwhile changed out bumper bar on aft PRS using parts from fwd PRS. Fixed broken electrical connection on aft PRS. Removed scaffolding from rig floor. Injected slop into F-14. Performed remaining pressure test on kill and choke manifolds. Modified hooks for lifting bridle. Changed o-rings on leaking coomey unit. Installed flush joint elevator on PRS and function tested same." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 4.0 hours. Operational details: Performed derrick inspection for potential dropped objects using CAN climbers." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Installed upper coupling cover on aft PRS. Greased couplings on fwd PRS." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.5 hours. Operational details: Greased couplings on aft and fwd PRS and worked on earth connections on aft PRS (discovered during derrick inspection). Meanwhile continued pressure testing choke manifolds." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Certified electrican and crew in use of cherry picker. Meanwhile performed ZMS adjustments for fox hole." "On 2008-11-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Continued to repair earth connections on aft PRS using cherry picker." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.2 hours. Operational details: Continued to repair earth connections on aft PRS using riding belt." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Greased aft PRS." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Held tool box talk for calibration /ZMS test of aft PRS. Meanwhile de-isolated PRS/DW/TDS. Calibrated blocks and draw work." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.2 hours. Operational details: Ran ZMS checks on aft PRS / TDS / aft iron roughneck / fwd PRS / HTS / PDM." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.2 hours. Operational details: Ran ZMS checks on aft PRS / TDS / aft iron roughneck / fwd PRS / HTS / PDM. Modified, installed and adjusted bumper bar on aft PRS." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: Held tool box talk prior to handling BHA. LO 12 1/4' BHA from derrick to deck. Cleaned and tidied rig floor." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.5 hours. Operational details: Held tool box talk prior to PU 8 1/2' BHA. PU and MU 8 1/2' BHA from surface to 68 m. Installed radioactive source. PU and MU 8 1/2' BHA from 68 m to 165 m." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Changed to PS21 and cleared rig floor." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 458m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: RIH with 8 1/2' BHA from 165 m to 458 m on 5' DP in singles. Experienced problems with fingerboard (slow respons on finger opening function)." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 581m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: RIH with 8 1/2' BHA from 458 m to 581 m on 5' DP. Had problems with elevator locking mechanism." "On 2008-11-12, at Well NO 15/9-F-15, a drilling event occurred at a depth of 581m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Broke circulation and filled pipe. Tested Schlumberger MWD tools." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 581m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Tested Schlumberger MWD tools and made a survey. Had ECD of 1.54 sg EMW. Could not close BX-elevator." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 581m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Changed out BX-elevator due to slack spring in closing mechanisme. Could not operate back-up elevator. Changed back to primary BX-elevator and decided to operated it while looking for a new latch locking pin spring." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1059m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: RIH with 8 1/2' BHA from 581 m to 1059 m on 5' DP. Filled DP every 10 stds. Had problems with elevator locking mechanism and experienced slow respons on joy-stick function for drawworks." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1059m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Replaced latch locking pin spring on BX-elevators. Fixed joy-stick for drawworks." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1390m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' BHA from 1059 m to 1390 m on 5' DP. Filled DP every 10 stds. Experienced problems with fingerboard (slow respons on finger opening function)." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1792m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: RIH with 8 1/2' BHA from 1390 m to 1792 m on 5' DP. Filled DP every 10 stds. Experienced problems with fingerboard (slow respons on finger opening function)." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1792m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Changed from 5' to 5 1/2' handling equipment." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2438m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: RIH with 8 1/2' BHA from 1792 m to 2438 m on 5 1/2 ' DP. Filled DP every 10 stds." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2476m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made up to TDS. Washed down from 2438 m to 2476. Parameters: Flow 1700 lpm / SPP 182 bar / String RPM 10 / TQ 7 kNm. MUD weight 1.44 SG." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2476m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Performed choke drill with crew." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2494m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: LO one 5 1/2' DP single for space-out. Continued to wash down from 2476 m and tagged TOC at 2494m (7 m below LC according to csg tally). Tagged with 2 MT, Parameters: Flow 1700 lpm / SPP 182 bar / String RPM 10 / TQ 7 kNm. MUD weight 1.44 SG." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2534m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Drilled out shoe track, 9 5/8' csg shoe found at 2534 m. Parameters: Flow 1700 lpm / SPP 198-210 bar / String RPM 10 / TQ 5-8 kNm. MUD weight 1.44 SG." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2539m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Cleaned out rathole and 3 m new formation to 2539 m. Parameters: Flow 1800 lpm / SPP 193 bar (rathole)-Flow 2100 lpm / SPP 252 bar (formation) / String RPM 20 / TQ 6-11 kNm. Started displacing to 1.35 SG OBM while drilling new formation." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2539m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Continued displacing well to 1.35 sg OBM, Flow 1800 lpm / SPP 165 bar at TD. Displaced choke & kill lines, filled sand traps and filled trip tank with 1.35 sg OBM." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2539m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Circulated until even mud weight 1.35 sg in/out. Pulled 8 1/2' BHA into 9 5/8' shoe track to verify no restriction." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2539m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: RIH and pumped 4 m3 LCM pill at 2539 m, Flow 1000 lpm / SPP 61 bar." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2440m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: POOH wet to 2440 m. Up weight 141 MT. Cleared drill floor." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2440m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.2 hours. Operational details: RU TIW, pump-in sub and cmt hose. Meanwhile held tool box talk for FIT. Lined up for pumping down both drill pipe and kill line. Closed pipe ram on BOP. Performed line test to 100 bar /10 min. 0.8% drop. Ok." "On 2008-11-13, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2440m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Took FIT equivalent to 1.60 SG, using 1.35 SG OBM. Pumped 70 lpm and applied 60 bars to the string and annulus. Shut down the pump." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2440m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Observed 0.75 bar drop (1.25%) in 10 min on FIT. Pressure levelled out. 367 ltrs pumped and 347 ltrs bled back. Downhole reading from Schlumberger equivalent to 1,613 SG." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2440m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: RD TIW, pump-in sub and cmt hose. Opened BOP pipe ram. Lined up for drilling. Pumped down hole and took survey at 2440 m." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2539m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 8 1/2' BHA from 2440 m to 2514 m on 5 1/2 ' DP. Performed kick drill / 55 sec. MU TDS and broke circulation. Staged up pumps and washed down to 2539 m, Flow 2200 lpm / SPP 235 bar / String RPM 40 / TQ 8-10 kNm. Up weight 142 MT / Down weight 121 MT / Free rotation weight 130 MT." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Sat power drive as per DD instructions. Drilled 8 1/2' hole from 2539 m to 2591 m. Parameters: Flow 2200 lpm / SPP 242-252 bar / String RPM 40 / Bit RPM 209 / TQ 10-12 kNm / ROP 19-25 m/hr. MUD weight 1.34-1.35 SG." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'drilling -- drill' and lasted for 12.8 hours. Operational details: Drilled 8 1/2' hole from 2591 m to 2883 m. Parameters: Flow 2200 lpm / SPP 241-246 bar / String RPM 80 / Bit RPM 209 / TQ 12-15 kNm / ECD 1.46-1.47 EMW / ROP 20-45 m/hr. MUD weight 1.35 SG. Started adding LCM according to plan 30 m above Ty formation." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Had 8 m3/hr losses in Ty formation at 2880-2883 m. Pulled off btm and flow checked well static. Ok." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'interruption -- well control' and lasted for 2.2 hours. Operational details: Staged up pumps to establish loss free rate. Meanwhile continued adding LCM chemicals to active and prepared 150 kg/m3 LCM pill in pit according contingency plan. Monitored losses while pumping and reciprocating pipe, Flow 440 lpm / SPP 25 bar / String RPM 10 / TQ 9-10 kNm. Average loss rate 1000 ltrs/hr." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2843m. The activity was categorized as 'interruption -- well control' and lasted for 1.8 hours. Operational details: Lined up and pumped 5 m3 LCM pill at 440 lpm. Spotted pill on TD at 2883 m. Pulled back one stnd to 2843 m while pumping the LCM pill out of the BHA." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2843m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Let LCM pill settle/soak. Monitored well on trip tank and rotated string with 5 rpm. No losses observed." "On 2008-11-14, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: RIH with 8 1/2' BHA to TD at 2883 m." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2876m. The activity was categorized as 'interruption -- well control' and lasted for 4.0 hours. Operational details: Circulated btms up at 440 lpm while monitoring for losses. Increased flow rate in steps of 200 lpm to 1200 lpm. Had losses 1-1.5 m3/hr. Increased flow rate to 1400 lpm and had losses 6 m3/hr." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2860m. The activity was categorized as 'interruption -- well control' and lasted for 1.5 hours. Operational details: Reduced flow rate to 600 lpm and monitored losses of 1 m3/hr while preparing second LCM pill with 200 kg/m3. Reciprocated string." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'interruption -- well control' and lasted for 0.5 hours. Operational details: RIH with 8 1/2' BHA to TD at 2883 m. Lined up and pumped 5 m3 LCM pill at 600 lpm." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'interruption -- well control' and lasted for 1.2 hours. Operational details: Continued pumping 5 m3 LCM pill at 600 lpm at TD. Pulled off btm and flow checked well. Static." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2735m. The activity was categorized as 'interruption -- well control' and lasted for 2.5 hours. Operational details: POOH with 8 1/2' BHA from 2842 m to 2735 m (above top of pill). Circulated, Flow 600 lpm / SPP 34 bar / String RPM 5 / TQ 8 kNm." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2735m. The activity was categorized as 'interruption -- well control' and lasted for 1.0 hours. Operational details: Pumped 4 m3 200 kg/m3 LCM pill, Flow 600 lpm / SPP 34 bar / String RPM 5 / TQ 8 kNm. Spottet pill on top of previous pill to cover all of Ty formation." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2670m. The activity was categorized as 'interruption -- well control' and lasted for 2.5 hours. Operational details: POOH with 8 1/2' BHA from 2735 m to 2670 m (above top of Ty formation). Staged up pumps to 1330 lpm and had 1 m3/hr losses that gradually was reduced down to zero." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2670m. The activity was categorized as 'interruption -- well control' and lasted for 2.8 hours. Operational details: Circulated and reciprocated pipe from 2670 m to 2641 m , Flow 1000 lpm / SPP 66 bar / String RPM 5 / TQ 5-7 kNm. Prepared for reducing mud weight down to 1.30 SG. Total loss since starting to loose mud on this section was approx 19 m3." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2670m. The activity was categorized as 'interruption -- well control' and lasted for 3.2 hours. Operational details: Bled into active to reduce mud weight from 1.35 SG to 1.30 SG. Meanwhile rotated and reciprocated pipe from 2670 m to 2641 m , Flow 1000 lpm / SPP 66 bar / String RPM 5 / TQ 5-7 kNm." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2670m. The activity was categorized as 'interruption -- well control' and lasted for 2.8 hours. Operational details: Staged up flow rate in 200 lpm increments to 1800 lpm above top LCM pill and monitored for losses. Had 1 m3/hr loss at 1600 lpm and 0.5 m3/hr loss at 1800 lpm." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'interruption -- well control' and lasted for 1.0 hours. Operational details: Lined up to trip tank and RIH from 2670 m to TD at 2883 m." "On 2008-11-15, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'interruption -- well control' and lasted for 1.0 hours. Operational details: Broke circulation and staged up flow rate to 600 lpm whilst displacing out LCM pill to skip. Had 0.5 m3/hr losses." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'interruption -- well control' and lasted for 2.0 hours. Operational details: Staged up flow rate in 200 lpm increments to 1000 lpm while continuing to displace out LCM pill. Had 0.5 m3/hr losses at 1000 lpm." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'interruption -- well control' and lasted for 3.0 hours. Operational details: Staged up flow rate in 200 lpm increments from 1000 lpm to 1800 lpm. Meanwhile rotated and reciprocated pipe from 2883 m to 2855 m. Had 0.5-1.0 m3/hr losses at all flow rates. Up weight 152 MT / Down weight 127 MT / Free rotation weight 138 MT (10 rpm)." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2883m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made connection. Staged up pump rate slowly to 1800 lpm. Started drilling 8 1/2' hole at 2883 m. Parameters: Flow 1800 lpm / SPP 166 bar / String RPM 80 / Bit RPM 218 / TQ 10-12 kNm / ROP 10 m/hr. MUD weight 1.30 SG." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2893m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 8 1/2' hole from 2883 m to 2893 m. Parameters: Flow 1800 lpm / SPP 167 bar / String RPM 80 / Bit RPM 218 / TQ 10-16 kNm / 1-2 MT WOB / ECD 1.38 EMW / ROP 10 m/hr. MUD weight 1.30 SG." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2893m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Stopped drilling due to 6 m3 losses/10 min. Discovered loss to be at shakers while changing screens. Changing screens was not communicated to drill floor." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2893m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Staged up pump rate slowly to 1800 lpm to start drilling ahead." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2915m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 8 1/2' hole from 2893 m to 2915. Parameters: Flow 1800 lpm / SPP 164 bar / String RPM 80 / Bit RPM 218 / TQ 11-13 kNm / 2-5 MT WOB / ECD 1.38 EMW / ROP 10 m/hr. MUD weight 1.30 SG." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2915m. The activity was categorized as 'interruption -- well control' and lasted for 1.8 hours. Operational details: PU off btm and reduced flow rate due to heavy losses of 36 m3/hr. Circulated at 450 lpm and staged up to find loss free rate at Flow 550 lpm / SPP 23 bar / String RPM 5 / TQ 5-6 kNm." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2915m. The activity was categorized as 'interruption -- well control' and lasted for 1.2 hours. Operational details: Pumped 5 m3 300 kg/m3 LCM pill at 550 lpm and spotted on btm/TD." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2775m. The activity was categorized as 'interruption -- well control' and lasted for 1.2 hours. Operational details: POOH with 8 1/2' BHA from 2915 m to 2775 m (above top of LCM pill)." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2775m. The activity was categorized as 'interruption -- well control' and lasted for 5.8 hours. Operational details: Staged up pumps in 200 lpm increments to 1800 lpm above top LCM pill at 2775 m. Had 0.7 m3/hr losses at 1800 lpm." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2914m. The activity was categorized as 'interruption -- well control' and lasted for 1.0 hours. Operational details: Lined up to trip tank. Flow checked well. Static. RIH from 2775 m to TD at 2915 m." "On 2008-11-16, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2913m. The activity was categorized as 'interruption -- well control' and lasted for 2.0 hours. Operational details: Broke circulation at 2914 m and staged up pumps in 200 lpm increments to 1000 lpm while rotating pipe." "On 2008-11-17, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2914m. The activity was categorized as 'interruption -- well control' and lasted for 3.0 hours. Operational details: Continued staging up pumps in 200 lpm increments from 1000 lpm to 1800 lpm while rotating and reciprocating pipe slowly. Had 0.5 m3/hr losses at 1800 lpm." "On 2008-11-17, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2932m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Drilled 8 1/2' hole from 2915 m to 2932 m. Parameters: Flow 1800 lpm / SPP 155-160 bar / String RPM 80 / Bit RPM 218 / TQ 10-11 kNm / 1-5 MT WOB / ECD 1.38 EMW / ROP 2-10 m/hr. MUD weight 1.30 SG." "On 2008-11-17, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3029m. The activity was categorized as 'drilling -- drill' and lasted for 14.0 hours. Operational details: Drilled 8 1/2' hole from 2992 m to 3029 m. Parameters: Flow 1800 lpm / SPP 157-188 bar / String RPM 80 / Bit RPM 218 / TQ 11-18 kNm / 1-9 MT WOB / ECD 1.38 EMW / ROP 2-10 m/hr. MUD weight 1.30 SG." "On 2008-11-17, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3051m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Drilled 8 1/2' hole from 3029 m to 3051 m. Parameters: Flow 2000 lpm / SPP 190-207 bar / String RPM 100 / Bit RPM 254 / TQ 12-15 kNm / 10-12 MT WOB / ECD 1.39 EMW / ROP 4-10 m/hr. MUD weight 1.30 SG." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3058m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8 1/2' hole from 3051 m to 3058 m. Parameters: Flow 2000 lpm / SPP 188-209 bar / String RPM 100 / Bit RPM 254 / TQ 12-15 kNm / 6-12 MT WOB / ECD 1.39-1.40 EMW / ROP 4 m/hr. MUD weight 1.30 SG. Had stick slip of more than 200%." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Worked with string rpm, ROP and WOB while drilling ahead from 3058 m to 3070 m to reduce stick slip. Parameters: Flow 2000 lpm / SPP 195-220 bar / String RPM 80-100 / Bit RPM 219-254 / TQ 11-20 kNm / 6-14 MT WOB / ECD 1.40 EMW / ROP 2-20 m/hr. MUD weight 1.30 SG. Observed 0.49% connection gas. Stick slip was found to be constant at 190% regardless of rpm, WOB and ROP." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8 1/2' hole from 3070 m to 3090 m. Parameters: Flow 2000 lpm / SPP 197-210 bar / String RPM 100 / Bit RPM 254 / TQ 12-16 kNm / 10-12 MT WOB / ECD 1.40 EMW / ROP 10-15 m/hr. MUD weight 1.30 SG. Observed 0.34 connection gas." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3088m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Circulated btms up while reciprocating pipe to clean hole before POOH to take pressure point. Flow 2000 lpm / SPP 186 bar / String RPM 100 / Bit RPM 254 / TQ 12 kNm. MUD weight 1.30 SG." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3081m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Continued circulating 2.5 x btms up while reciprocating pipe to clean hole before POOH to take pressure point. Flow 2000 lpm / SPP 178 bar / String RPM 100 / Bit RPM 254 / TQ 11-14 kNm. MUD weight 1.30 SG." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3060m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: Held tool box meeting prior to performing logging and taking pressure points. Logged out of hole from 3081 m to 3060 m at 20 m/hr. Up weight 155 MT / Down weight 123 MT." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3010m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: POOH with 8 1/2' BHA from 3060 m to 3010 m." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3010m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: Performed stick test at 3010 m with pumps on, Flow 2000 lpm / SPP 176 bar. Pulled up to 3006 m and took first pressure point at 2608 m TVD (probe depth), Flow 2000 lpm / SPP 221 bar. Formation pressure was 0.86 SG." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2946m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: POOH with 8 1/2' BHA from 3006 m to 2947 m. Up weight 157 MT / Down weight 122 MT." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2946m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.2 hours. Operational details: Took second pressure point at 2583 m TVD (probe depth), Flow 2000 lpm / SPP 218 bar. Performed down link. Formation pressure was 0.86 SG." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3083m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.8 hours. Operational details: RIH with 8 1/2' BHA from 2946 m to 3083 m." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3090m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Established drilling parameters prior to drilling ahead. Washed down from 3083 m to 3090 m, Flow 1100 lpm / SPP 66-71 bar." "On 2008-11-18, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3180m. The activity was categorized as 'drilling -- drill' and lasted for 10.0 hours. Operational details: Drilled 8 1/2' hole from 3090 m to 3180 m. Flow 1800-2000 lpm / SPP 171-214 bar / String RPM 100-160 / Bit RPM 254-299 / TQ 13-24 kNm / WOB 7-15 MT / ECD 1.40 EMW / ROP 10-24 m/hr. MUD weight 1.30 SG. Performed fingerprint measurements while drilling from 3090 m to 3097 m at 14:30 - 16:00 and from 3168 m to 3183 m at 23:00 - 00:30." "On 2008-11-19, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3272m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole from 3180 m to 3272 m. Flow 2000 lpm / SPP 213-222 bar / String RPM 100 / Bit RPM 254 / TQ 13-23 kNm / WOB 10-13 MT / ECD 1.40-1.41 EMW / ROP 20 m/hr. MUD weight 1.30 SG. Added 8 m3 of Baralube to active at 00:30. Performed fingerprint measurements while drilling from 3319 m to 3231 m at 02:30 - 03:30." "On 2008-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 8 1/2' hole from 3488 m to 3569 m. Flow 2000 lpm / SPP 213-218 bar / String RPM 100 / Bit RPM 254 / TQ 14-24 kNm / WOB 10-15 MT / ECD 1.41 EMW / ROP 20 m/hr. MUD weight 1.30 SG. Up weight 170 MT / Down weight 127 MT / Free rotational weight 143 MT. Pulled off btm due to rapide increase in SPP from 215 bar to 230 bar at 3498 m. Had SPP of 190 bar off btm. Lost communication to C-link at 3548 m." "On 2008-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3655m. The activity was categorized as 'drilling -- drill' and lasted for 13.0 hours. Operational details: Drilled 8½' hole from 3569 m to 3655 m. Flow 2000 lpm / SPP 209-222 bars / String RPM 80-100 / Bit RPM 236-254 / TQ 10-23 kNm / WOB 13-16 MT / ECD 1.41-1.45 EMW / ROP 5-12 m/hr. MUD weight 1.30-1.35 SG. Up weight 170 MT / Down weight 127 MT / Free rotational weight 143 MT. Increased the mud weight in steps from 1.30 to 1.35 SG. When weighing up the mud. Observed loses of 4m³/hour, gradually reduced to 0 when drilling ahead." "On 2008-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3670m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Drilled 8½' hole from 3655 m to 3670 m. Flow 2000 lpm / SPP 220-230 bar / String RPM 80 / Bit RPM 236 / TQ 14-17 kNm / WOB 10-14 MT / ECD 1.45-1.46 EMW / ROP 3-13 m/hr. MUD weight 1.35 SG. Up weight 170 MT / Down weight 127 MT / Free rotational weight 143 MT." "On 2008-11-20, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3670m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.2 hours. Operational details: Circulated hole clean reciprocating the string. 2000 lpm / SPP 203 bars." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3670m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Continued circulating the hole clean at 2000 lpm / SPP 203 bars." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3670m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Performed flow check to static well, with slow rotation 5 rpm." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3403m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: POOH 5 std 5½' DP wet from 3670 m to 3403 m." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3403m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped 5 m³ 1.75 SG slug." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3243m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued to POOH with 5½' DP form 3403 to 3243 m. Attempted setting 5½' DP std in finger board. Pipe did not enter the finger board and got bent." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3243m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Investigated the 5½' DP std and prepared securing of the 5½' DP std. Performed SJA and commenced securing of the 5½' DP std. Simultaneously reciprocated and rotated the string 10 rpm." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3243m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Secured bent 5½' DP std in finger board. Inspected the AFT PRS." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2519m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Held tool box talk with day shift and continued to POOH with 8½' BHA on 5½' DP from 3243 m to 2519 m into the 9 5/8' shoe." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2519m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well - static. Performed kick drill 45sec. Serviced the TDS." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2519m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Flushed choke & kill line through BOP. Meanwhile serviced & inspected the TDS." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1792m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Continued to POOH with 8½' BHA on 5½'DP from 2519m to 1792m." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1792m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Held tool box talk and changed to 5' DP handling equipment. Laid out x/o." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- trip' and lasted for 2.8 hours. Operational details: Continued to POOH with 8½' BHA on 5' DP from 1792m to 165 m." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 165m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Flow checked well - static. Meanwhile checked dies on FWD PRS, removed PS 21 slips." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 78m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: Held tool box talk and started to lay out 8½' BHA. Cleared & cleaned drill floor. Prepared & removed radio active source from Ecoscope tool." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: Held tool box talk with night shift and continued laying out 8½' BHA." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Cleared drill floor. Held tool box talk prior to lay out bent 5½' DP std." "On 2008-11-21, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Laid out bent 5½' DP." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.2 hours. Operational details: Picked up jet sub. Ran in and jet washed the BOP. Picked up the test plug. RIH and jet washed the WH. Landed of test plug." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Held tool box talk prior to perform BOP test. Made up pup jnt and swadge to TDS." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: Started pressure testing of the BOP 345 bars." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 5.2 hours. Operational details: Continued to pressure test BOPs as per procedure, 30/345 bars 5/ 10 mins. Meanwhile pressure tested upper lower IBOPs & Kelly hose." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- wait' and lasted for 1.0 hours. Operational details: Left drill floor due to exhaust (CO levels @ 60 ppm), monitor area until clear reading on sensors." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: Held tool box talk and broke test assembly from TDS, laid out same." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Checked dies on PRS, cleaned & cleared drill floor prior to pick up BHA #2. BX elevator not operating probably." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Changed out BX elevators due to latching problem, back up set would not work, installed original elevator & investigated problem with latch." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Held tool box talk and started to pick up 8½' BHA." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Held tool box talk and loaded the radio active source to Ecoscope assembly." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Changed BX inserts to 5' DP. Continued to RIH with 8½' BHA to 180m." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed out master bushing to PS 21 slips." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 992m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued to RIH with 8½' BHA on 5' DP from 180m to 992m." "On 2008-11-22, at Well NO 15/9-F-15, a drilling event occurred at a depth of 992m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Made up X-over to 5½'. Filled the DP, Staged up pumps until static active volume was established, prior to test of MWD." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 992m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: Staged up pumps until communications with MWD tool was established, required 2 mud pumps, 1730 l/m." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1980m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued to RIH with 8½' BHA on 5' DP from 992m to 1980m. Filling the DP every 10 std." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1980m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held tool box talk and installed x-over to 5½''. Filling the DP. Changed inserts in elevators and PS21." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2534m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued to RIH with 8½' BHA on 5½' DP from 1890m to 2534 m. Filling the DP every 10 std." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2534m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Changed out PS21 slips to master bushing. Prepared for changing out the wash pipe." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: Trouble shoot problem to activate permit, SAP system down." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Started changing out wash pipe." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Continued to change out wash pipe." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Removed TIW valve. Made up to TDS, broke circulation and circulated bottoms up at shoe. Staged up pump rate in 10 spm increments, while monitoring for losses. Meanwhile made up TIW & grey valves & rigged up for pressure testing. Stopped rotation, serviced AFT PRS, TDS and travelling block." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued to circulate with flow rate at 1600l/m , while servicing the TDS & travelling block." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: De-isolated equipment PRS/TDS. Monitored well on Trip Tank, observed increase in Trip Tank." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Shut well in, standpipe press 0 SICP 0, opened choke and flow checked. Measured returns with decreasing trend." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Lined up and flushed across BOP, opened upper pipe rams." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2532m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Flow checked on Trip tank. Meanwhile held tool box talk and installed PS-21 slips." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3581m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Continued RIH from 2532mt to 3581m filling the pipe every 10 std." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3581m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Broke circulation, staged up flow rate & RPM in 10 spm increments & monitored for losses. Established loss free circulation rate to 1700 l/m / 20 rpm / SPP 160 bars. Added 3 sacks/ hour of LCM." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3616m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Took survey at 3616m." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- survey' and lasted for 1.2 hours. Operational details: Continued to RIH while logging to 3632m, 30 m/hour, 1500 l/m, 60 rpm increased to 120 rpm due to stick slip, max ECD 1.46 sg EMW. Got downhole losses 12 m³/hour. Stopped RIH, cut back pumps and rpm." "On 2008-11-23, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Started to establish loss free pump rate." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3632m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Continued to establish pump rate - 1500 l/m and 80 rpm with losses, 3-4 m³/h." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- survey' and lasted for 1.8 hours. Operational details: RIH while logging from 3626 m to 3660m at 20 m/hour, 80 rpm, 1500 l/m, max ECD 1.46 sg EMW. Losses increased to 8m³/hour and SPP picked up. Mud weight in return uneven, max 1.38 SG." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.8 hours. Operational details: Conditioned the mud weight to 1.35 SG with 800-1000 l/m, 52-62 bars SPP, 10 rpm." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Conditioned the mud weight to 1.35 SG with 800 l/m, 52 bars SPP, 10 rpm." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: Continued to condition mud, attempted to stage up pump rate. Monitored for losses, average losses 3½ m³/hour @ 1300 lpm." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Lined up pit #13 & pump 8½ m³ LCM pill. Staged up flow rate to 1300 lpm & monitored loss rate. Circulated LCM pill out of hole to skips. Average losses 3½ m³. Meanwhile prepared equipment for pulling wet." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Flow checked well, observed rapid increase to Trip Tank, shut in well on upper rams, monitored pressure built up SIDP 0bar (float installed), SICP 6,7 bars. 11:50 bled off approx 1m³ from well and closed in, SICP 5,0 bar - no pressure built up. 12:18 bled off additional 2.75 m³ from well and closed in, SICP 3,2 bars - no pressure built up. As no pressure built up to original SICP was observed, conclusion is supercharged formation. Continued to bleed off from well, observed decreasing trend in flow back and decided to open BOP. Total volume bled back from well: 4½ m³." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Flushed across BOP prior to open up pipe ram. Broke circulation, staged up to 20 RPM, staged up mud pumps to 800lpm. Decided to cut mud weight. Bled into active to reduce mud weight to 1.32 SG. Circulated to even mud weight. Total losses approx. 5½ m³." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3640m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Continued to circulate and condition mud to even mud weight 1.32 SG." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3640m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Stopped pumps and monitored return flow. Active volume increased 2.45 m³ when pumps turned off." "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3640m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: Monitored returns on Trip Tank rotating the string 5 rpm. Flow reducing over time. Table below. Time Actual gain Gain 21.00-21.15 0.51 m³ 2.04 m³/h 21.15-21.30 0.51 m³ 2.04 m³/h 21.30-21.45 0.20 m³ 0.80 m³/h 21.45-22.00 0.13 m³ 0.52 m³/h 22.00-22.15 0.09 m³ 0.36 m³/h 22.15-22.30 0.08 m³ 0.32 m³/h 22.30-22.45 0.06 m³ 0.24 m³/h 22.45-23.00 0.04 m³ 0.16 m³/h 23.00-23.15 0.03 m³ 0.12 m³/h 23.15-23.30 0.03 m³ 0.12 m³/h" "On 2008-11-24, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3540m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Started to POOH wet from 3640m to 3540m." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2922m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Continued to POOH wet from 3540m to 2922m. Made up to TDS." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2922m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pumped LCM pill 10.2 m³ 335kg/m³, displaced with 1.32 SG mud 30 m³ at 800 l/m." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2655m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Started to POOH wet from 2922m to 2655m. Well stable as pulling out." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2649m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Continued to pull out to 2649m. Staged up flow rate in increments to establish loss free rate, with 5 rpm on string." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2649m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 7.5 hours. Operational details: Continued to stage up flow rate to 1750 lpm, to establish loss free rate. Staged up RPM from 10 to 160, continued monitoring for losses. Initial loss rate 3.7m³/hour at 1750l/m. Observed decrease in loss rate while stepping up RPM from 100 to 160. Final loss rate 800 lpm at 1750 lpm / 160 rpm with decreasing trend, total losses 12.3m³. Final ECD 1.29 sg EMW. Staged down flow rate & RPM in increments of 10 SPM & 10 RPM." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2649m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Flow check prior to RIH." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Broke off TDS, RIH from 2654m to 3660m filling every 10 stds. No losses downhole." "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: Staged up pumps to 1000 l/m, circulated out LCM pill. Staged up RPM to 30. Circulated two times bottoms up. Max ECD 1.37 sg EMW. Time Actual loss m³ Loss m³/hour 19,45-20,00 0,56 2,24 20,00-20,15 1,87 7,48 20,15-20,30 1,79 7,16 20,30-20,45 1,55 6,2 20,45-21,00 1,5 6 21,00-21,15 0,1 0,4 21,15-23,15 0,8 0,4" "On 2008-11-25, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.8 hours. Operational details: 2315-0000 Staged up pumps 1100 - 1300 lpm at RPM 30, for drilling parameters. Observed loss rate. LCM pill still coming over shakers. ECD at 1300 lpm: 1.38 sg EMW. Time Actual loss m³ Loss m³/hour 23,15-23,30 1,5 6 23,30-23,45 0,25 1 23,45-00,00 0,24 0,96" "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3660m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.8 hours. Operational details: Continued staging up pumps 1300 - 1700 lpm and RPM 30-120, for drilling parameters. Observed loss rate. LCM pill still coming over shakers. Max ECD 1.40 sg EMW. Time Actual loss m³ Loss m³/hour 00,00-00,15 0,16 0,64 00,15-00,30 0,15 0,6 00,30-00,45 1,04 4,16 00,45-01,00 0,68 2,52 01,00-01,15 0,2 0,8 01,15-01,30 0,15 0,6 01,30-01,45 0,74 2,96" "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3662m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Took survey and connection, 6,8 m³ flow back observed over connection." "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3670m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Logged as RIH, 1485 l/m, 20 ROP, 60rpm from 3662m to 3670m. ECD 1.39 sg EMW." "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3682m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: Started drilling and brake in new bit. Drilled 8 1/2' hole from 3670 m to 3682.5m. Flow 1700 lpm / SPP 145-150 bars / String RPM 80-160 / / TQ 12-20 kNm / WOB 4-11 MT / ECD 1.38-1.42 EMW / ROP 3-10 m/hr. MUD weight 1.32 SG. Averaged losses 2,6 m³/hour." "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3734m. The activity was categorized as 'drilling -- drill' and lasted for 5.2 hours. Operational details: Continued drilling 8½' hole from 3682.5 m to 3734 m. Flow 1700 lpm / SPP 150 bars / String RPM 160 / TQ 16-22 kNm / WOB 5-9 MT / ECD 1.42-1.43 EMW / ROP 10-20 m/hr. MUD weight 1.32 SG. Losses 2-3 m³/hr" "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3734m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pulled off bottom and circulated to clean hole, due to increasing trend in losses, loss rate increased to approx. 6 m³/hr. ECD 1.43 SG EMW. Meanwhile discussed further plan with onshore organisation." "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3785m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: Continued drilling 8½' hole from 3734 m to 3785 m. Flow 1700 lpm / SPP 155 bars / String RPM 180 / TQ 16-22 kNm / WOB 5-9 MT / ECD 1.42 EMW. MUD weight 1.32 SG. Controlled ROP at 10 m/hr. Connection at 13:30, 3743 m, 9.3 m³ returns over connection period. 1,14 m³/min. Connection at 18:00, 3785 m, 7,9 m³ returns over connection period. 1,69 m³/min. Average losses 1,4 m³/hr" "On 2008-11-26, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3834m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Continued drilling 8½' hole from 3734 m to 3834 m. Flow 1700 lpm / SPP 155 bars / String RPM 180 / TQ 16-19 kNm / WOB 1-4 MT / ECD 1.42 EMW. MUD weight 1.32 SG. Controlled ROP at 10 m/hr. Up weight 171 MT / Down weight 121 MT / Free rotational weight 137 MT. Connection at 22:15, 3823 m, 13,5 m³ returns over connection period. 1,32 m³/min. Average losses 1,4 m³/hr" "On 2008-11-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3889m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued drilling 8½' hole from 3834 m to 3889 m. Flow 1700 lpm / SPP 155 bars / String RPM 180 / TQ 14-16 kNm / WOB 1-2 MT / ECD 1.42 EMW. MUD weight 1.32 SG. Controlled ROP at 10 m/hr. Up weight 173 MT / Down weight 125 MT / Free rotational weight 144 MT. Connection at 03:15, 3864 m,10.7m³ returns over connection period. 1,29 m3/min. Losses per hour from 00:00 hrs to 01:45 average 1,4 m³/hr. Losses per hour from 01:45 hrs to 05:00 average 1,2 m³/hr." "On 2008-11-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4008m. The activity was categorized as 'drilling -- drill' and lasted for 5.8 hours. Operational details: Continued drilling 8½' hole from 3955 m to 4008 m. Flow 1700 lpm / SPP 155 bars / String RPM 180 / TQ 14-16 kNm / WOB 4-6 MT / ECD 1.42 EMW. MUD weight 1.32 SG. Controlled ROP at 10 m/hr. Up weight 173 MT / Down weight 128 MT / Free rotational weight 148 MT. Connection at 3986m, 9.0m³ gains, 1.6% max connection gas observed. 2,25m³/min." "On 2008-11-27, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4050m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Continued drilling 8½' hole from 4008 m to 4050 m. Flow 1700 lpm / SPP 158 bars / String RPM 180 / TQ 16-18 kNm / WOB 1-2 MT / ECD 1.42-1.43 EMW. MUD weight 1.32 SG. Controlled ROP at 10 m/hr. Up weight 173 MT / Down weight 128 MT / Free rotational weight 148 MT. Average losses 1.5 m³/hr. Connection at 4026m, 11.8m³ gains, 1.9% max connection gas observed. 1.18m³/min." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4064m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued drilling 8½' hole from 4050 m to 4064 m. Flow 1700 lpm / SPP 158 bars / String RPM 180 / TQ 16-18 kNm / WOB 1-3 MT / ECD 1.43 EMW. MUD weight 1.32 SG. Controlled ROP at 10 m/hr. Average losses 1.65 m³/hr. Tagged stringer at 4064mMD/3160m TVD." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4067m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled through stringer with reduced WOB/RPM 5MT/120. Flow 1700 lpm / SPP 158 bars / String RPM 120 / TQ 16-20 kNm / WOB 5 MT / ECD 1.43 EMW. MUD weight 1.32 SG. Average losses 1.65 m³/hr. Connection at 4067m, 10.3m³ gains, No connection gas observed. 1.71m³/min." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4090m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued drilling 8½' hole from 4067 m to 4090 m (TD). Flow 1700 lpm / SPP 160 bars / String RPM 180 / TQ 16-18 kNm / WOB 2-11 MT / ECD 1.43 EMW. MUD weight 1.32 SG. Controlled ROP at 10 m/hr. Up weight 173 MT / Down weight 128 MT / Free rotational weight 148 MT. Average losses 4.7 m³/hr." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4060m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Pulled of bottom started circulating hole clean reciprocating the string. Zero rpm pulling up and 80 rpm working down, pump rate to 1850 lpm / SPP 180 bars / ECD 1,42 EMW. Average losses 0.5m³/hr." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4080m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Continued circulating hole clean reciprocating the string. Zero rpm pulling up and 80 rpm working down, pump rate to 1850 lpm / SPP 180 bars / ECD 1,42 EMW. 1.8m³ gain." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4080m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Monitored well on Trip Tank, 9.3m³ gain, shut well in when the flow was at a rate of 8.4m³/hr." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4080m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Closed upper pipe rams, line up to fwd choke. Monitored pressure increase on fwd choke, up to 5.2bars. Opened choke and bled off approx 0,20m³. Closed choke and monitored pressure increase on fwd choke, up to 4.8bars. Opened choke and bled off approx 0,29m³. Closed choke and monitored pressure increase on fwd choke, up to 4bars. Opened choke and bled off monitoring returns through sample line, flow decreased from 20l/min to 10l/min. Flushed kill and choke lines, opened upper pipe rams." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4080m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flow checked - well static." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4080m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Dropped Gyro and pumped down same at 780 lpm." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4080m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed Gyro rotation shots at 4087m." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3256m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Pumped out of hole from 4087m to 3256m, 20m/min, 730lpm. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 3256m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed Gyro rotation shots at 3256m." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2932m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Pumped out of hole from 3256m to 2932m, 20m/min, 730lpm. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2695m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued pump out of hole from 3932m to 2695m, 20m/min, 730lpm. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2695m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Performed Gyro rotation shots at 2695m." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued pump out of hole from 2695m to 2531m, 20m/min, 730lpm. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Circulated at shoe. Checked gas levels - ok. No excessive gas reading from BTM up. Meanwhile service TDS." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Flow checked well on trip tank. Well - static." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pumped 5 m³ of 1.62 SG slug. Allowed to settle." "On 2008-11-28, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2251m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH on elevators from 2531m to 2251m. N.B. restricted pulling speed to allow hole to take correct volume and Gyro restrictions. Due to Gyro, pipe to be stationary in slips for 2 min. before continued POOH. Tripping speed 373 m/hr." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2251m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Perform Gyro rotation shots at 2251m." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1885m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued POOH from 2251m to 1885m. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH. Tripping speed 488 m/hr." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1885m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Changed out handling equipment from 5½' to 5'." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1724m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued POOH with 5' pipe from 1885-1724m. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH. Tripping speed 322 m/hr." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1724m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Perform Gyro rotation shots at 1724m." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1194m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued POOH with 5' pipe from 1724m to 1194m. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH. Tripping speed 424 m/hr." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1194m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Perform Gyro rotation shots at 1194m." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 706m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued POOH with 5' pipe from 1194m to 706m. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH. Tripping speed 488 m/hr." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 706m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Perform Gyro rotation shots at 706m. Problems with PS-21 slip." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 706m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: PS-21 slips unable to hold DP. Investigated problem." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 706m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Repaired PS-21 slips." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued POOH with 5' pipe from 706m to 217m. Due to Gyro, pipe to be stationary in slips for 2 min. before continue POOH." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Flow checked - well static. Meanwhile reset Diagnostic work station, serviced and maintenance on AFT PRS." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: Continued POOH with 5'' HWDP and 8½' BHA. Laid out BHA." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pulled radioactive source to rig floor and removed from BHA into safe container." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued laying down 8½' BHA." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Cleared rig floor." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Rigged up to RIH with 3½'' Drill pipe." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: Held tool box talk and RIH with 3½'' Drill pipe from surface to 250m, in singles picked up from cantilever. Tripping speed 143m/hr" "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed to 5'' handling equipment." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1676m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: RIH with 5'' Drill Pipe from 250m to 1676m. Tripping speed 713m/hr" "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1676m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held tool box talk, performed checks and emptied trip tank." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1961m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH with 5'' Drill Pipe from 1676m to 1961m. Tripping speed 570m/hr." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1961m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed to 5½' handling equipment." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2534m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIH with 5½'' Drill Pipe from 1961m to 2534m. Reduced running speed due to hole not taking correct volume. Tripping speed 573m/hr." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2648m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH open hole from 2534m to 2648m. Performed kick drill 41 sec." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2648m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flow checked well on trip tank, 670l gain in 7 minutes." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2648m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Shut in well on UPR pipe ram. Monitored pressure build up on choke. No pressure build up seen. Heavy rain, rain water into well 6 l/min." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2648m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Opened choke and flow checked with fully open choke - well static." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2648m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flushed across BOP prior to opening same." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2648m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Broke out FOSV and made ready for tripping." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2648m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up to run in on active pit due to large amounts of rain water going into mud." "On 2008-11-29, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2884m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued RIH from 2648m to 2884m." "On 2008-11-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4061m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: Continued RIH from 2884m to 4061m." "On 2008-11-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4086m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U TDS, establish circulated at 500 LPM. Washed down from 4061m and tagged TD @ 4091m. SPP increased from 23 bars to 28 bars. P/U 5 m off btm to 4086m." "On 2008-11-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4086m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.5 hours. Operational details: Started to circulation. Increased rate from 500 lpm to 1500 lpm, observed max loss rate 6 m³/hr. Beamed back the rate to 1250 lpm 77 bars. Total losses during circulation 4.3m³. Maximum gas at bottoms up 2%. Meanwhile held pre-job meeting prior to perform cement job." "On 2008-11-30, at Well NO 15/9-F-15, a drilling event occurred at a depth of 4086m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Attempted to pressure test line from cmt unit to standpipe on rig floor. No go due to minor cmt pump issue and wash pipe failure." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2633m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Lined up from cement unit to string. Mixed & pump 9,75 m³ of 1,90 SG slurry @ 800 LPM." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2633m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Displaced cement with rig pump 1.32 SG OBM 1250 lpm. After 15.5 m³ pumped catch up with cement and pump pressure increased to 44 bars. Total displacement volume 20.9m³. Lost 3.9m³ during displacement." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2350m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Held tool box talk and POOH from 2633m to 2350m. Pulled dry w/ 2-3 min/std. through cement plug." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2350m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Pumped 2,5m³ 1,32sg OBM at 2350m to clean stinger." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued POOH from 2350m to 2034m. Tripping speed 632 m/hr." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 4.2 hours. Operational details: Loaded 2x sponge balls and circulated with 1,32sg OBM, 120 rpm/1000 lpm observed losses (1.6m³). Reduced to 120 rpm/500 lpm. Circulated w/ stable returns until cement plug set up." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Monitored well on trip tank. Well - static." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Racked back one stand. Conducted kick drill 50 sec." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flushed manifold after cement job. While hanging off the TDS block." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'interruption -- maintain' and lasted for 2.2 hours. Operational details: Slip and cut drill line." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped slug 7.8m³ 1.68 SG chased with 3.6m³ of 1.32 SG OBM. Simultaneously changed out master bushing to PS-21 slips." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Function tested BOP." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1961m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Racked last stand 5½' DP, broke out and laid out X-over." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1310m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Continued POOH from 1961m to 1310m. Tripping speed 434 m/hr." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1310m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk with crew. Checked Iron roughneck, pipe handler, elevator and PRS dies." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Continued POOH with 5' DP from 1310m to 250m. Monitored well on trip tank. Tripping speed 707m/hr" "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 250m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed out handling equipment from 5'-3½'." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH with 3½' DP, laid out singles from 250-241m. HTS roller failed." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: HTS rollers failed to stop. As running HTS and Rollers in manual. Rollers did not stop after command. This caused 3½' DP to tip off the last Roller post. The DP end landed on the Cantilever. No personnel in area due to area had been barried prior to commencing operation. Installed FOSV and monitored on trip tank." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Barried off operation area on drill floor and cantilever. Investigated incident. Documented incident by taking pictures." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held tool box talk and removed the 3½' DP from HTS rollers." "On 2008-12-01, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Maintenance team investigated the causes." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Continued investigation of the incident. Simulated incident. Found HTS rollers got stop signal but had too long slowing down period. Investigated for hydraulic or electrical error. On 2nd simulation attempt the system worked normal, rollers stopped as they should. Unable define the error." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 241m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Held tool box talk and removed the HTS rollers." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: Continued POOH with 3½' DP from 241m to surface and laid out 3½' DP on cantilever." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Held tool box talk and leak tested Cement line to rig floor 200 bars/5mins. Attempted to pressure test the 2nd cement plug. Pressure up against shear ram 50 bars and increased pressure in 20 bars increments. At 110 bars pressure drop rapid to 70 bars. 0.95 m³ pumped 0.6 m³ return. Trip tank steady." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Prepared for RIH with 8¼' drill out BHA." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: Prepared for RIH with 8¼' clean out BHA." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 125m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: RIH with 8¼'' clean out BHA. Removed nozzles in bit." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 125m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed out master bushing to PS21 slips." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1510m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.5 hours. Operational details: RIH with 5'' Drill pipe from 125m to 1510m. Filling pipe every 10 stands. Closed end displacement, monitoring returns on trip tank. Tripping speed 395 m/hr. 5'' elevators not closing probably on 5'' drill pipe." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1510m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Investigated slipped stand in PRS and elevator." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1836m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Continued RIH with 5' DP from 1510m to 1836m. Tripping speed 326 m/hr." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH from 1836m to 2034m, up/down weight 129/112 MT. Tripping speed 198 m/hr." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2034m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.8 hours. Operational details: Started circulation, staged up pumps from 450 to 2000 L/min, SPP 21.5 to 99.4 bars." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2401m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.2 hours. Operational details: Washed down from 2034m to 2401m, down/up weight 114/131 MT. 2000 L/m, 105bar, increased pumprate to 2500 L/m, 167bar. No cement over the shakers." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2631m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 3.0 hours. Operational details: Continued washing down from 2401m to 2587m w/ 2500 lpm, SPP 167-175bars. Tight/overpull at 2587mt. Started rotation at 20rpm. Continued to wash/ream down from 2587m to 2629, Torq 5-10 kNm. Occasionally WOB at 5 mt for a few seconds, otherwise no WOB. Took weight at 2629m 10 MT. Washed through. Reamed to 2631 m. Stopped rotation and set down 10 MT with 2500 lpm, firm cement at 2631m (TD). 50/50 cement/formation over the shakers. No gain/losses during clean out." "On 2008-12-02, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2621m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: Circulated hole with 2500 lpm 80 rpm and reciprocated the string. Size of the cutting in return: Cement Ø1' and formation chips 2' x ½' x 1/8'. Circulated 3 bottoms up. After 2nd bottoms up 90 % formations cuttings back. No gain/losses during clean out. Decided to pump out to 9 5/8' casing shoe." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2521m. The activity was categorized as 'plug abandon -- wait' and lasted for 0.5 hours. Operational details: Drill crew supplied with stretcher team to carry person from hospital to the hellideck. Meanwhile slowly pumped out of open hole w/2500 LPM." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2521m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.8 hours. Operational details: Pulled out into the shoe at 2521m pumping." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2521m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated hole clean inside the shoe at 2500 lpm no rotation. 2 bottoms up before hole clean. Meanwhile serviced TDS. Problem with trip tank." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2521m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Lever difference in trip tank. Investigated same." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2521m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Flow checked well static." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2521m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 8 m³ slug 1.71 SG OBM chased with 3.6m³ SG OBM, at 670 lpm 26 bars." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2359m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Started to POOH from 2521m to 2359m. Observed a 0,5 m3 gain. Tripping speed 324 m/hr." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2359m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flow checked well - static." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1839m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued POOH from 2359m to 1839m. Tripping speed 1040 m/hr." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1839m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Changed to 5' handling equipment." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1470m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued POOH from 1839m to 1470m. Tripping speed 738 m/hr." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 125m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Continued POOH from 1470m to 125m. Tripping speed 896 m/hr." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 125m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flow checked prior to lay out BHA - static. Simultaneously changed out PS21's to master bushing." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 125m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Hold tool box talk and racked back/laid out BHA. Problem with BX elevator." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 125m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Investigated leak on BX elevators and repaired same." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued to laying out BHA." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleared rig floor." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Rigged up prior to pick up 3½' DP. Tested HTS rollers." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: Boat in. Waited for crane." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: Picked up and ran in 3½' DP from surface to 299m." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 299m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed to 5' handling equipment." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2009m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.5 hours. Operational details: RIH from 299m to 2009m. Pump 1m³ every 500m to ensure 3½' not plugged. Tripping speed 488 m/hr." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2009m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed to 5½' handling equipment." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2530m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH from 2009m to 9-5/8' shoe at 2530m. Tripping speed 694 m/hr." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2631m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.5 hours. Operational details: Washed down from 9-5/8' shoe to 2638m at 2500 lpm, 233 bars. Did not tag previous TD at 2631m. No pressure increase in SPP or weight difference as washing down." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2631m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Pulled up to 2631m. Continued circulating with 2500 lpm, 233 bars and 100-120 rpm, reciprocating the string. Some cuttings over shakers. No gain or losses during circulation. Meanwhile prepared 6m³ 1.34 SG WBM Hi-vis pill. Problem with mixing the pill." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2631m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Problem with mixing. Found hopper blocked and cell feeder did shut off." "On 2008-12-03, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2631m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.2 hours. Operational details: Mixed and prepared 6m³ 1.34 SG WBM Hi-vis pill." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2631m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 6m³ 1.35 SG WBM Hi-vis pill at 670 lpm, 33bars. Displaced pill with 1,34 SG OBM 2500 lpm 230 bars." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2584m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: POOH from 2631m to 2584m." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2584m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.8 hours. Operational details: Circulated bottoms up with 1.34 SG OBM, 2500 lpm 230 bars, 120 rpm. After 79m³ pumped observed excess Hi-vis pill at the shakers. Continued circulate to clean shakers. Meanwhile held tool box talk prior to set the 3th cement plug." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2584m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.2 hours. Operational details: Lined up from cement unit through standpipe and TDS. Closed stand pipe valve and pressure tested line up from cement unit against standpipe valve to 200 bar." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2584m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pumped 9.6 m³ of 1.60 SG spacer at 2000 lpm, 106 bars. Chased the spacer with 2 m3 1.34 SG OBM." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2584m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Mixed and pumped 12.04 m³ 1.90 SG G-cement at 800 lpm, 51-23 bars. Displaced cement to rig floor with 892 litres Drill water." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2584m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Displaced cement plug with mud pumps. 19.7m³ 1.34 SG OBM at 2000 lpm, 30 rpm. After 4.4m³ pumped catch the cement. After 460 strokes pumped pulled the string 1m up, while pumping." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2229m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: POOH 2-3 min/stand to 2229 m. Pulled dry. Pumped 1m³ 1.34 SG OBM at 500 LPM to remove the excess cement inside 3½' DP." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2127m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Continued POOH from 2229 m to 2127m. Problem with PRS." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2127m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Investigated fault with PRS. Found VFD Variable frequency drive fault. Fault reset." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2008m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Continued POOH from 2127 m to 2008m." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 2008m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed to 5' handling equipment." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1928m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH with cement stinger on 5' DP from 2009 m to 1928 m MD. Trip speed 162 m/hrs." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1928m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pumped 2 ea sponge balls to clean pipe at 2000 lpm / SPP 140 bar / 120 rpm / torque 3-7 kNm." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1928m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Flowchecked well on triptank - well static." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1928m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pumped 5 m3 og 1,7 sg slug and chased same to drillfloor. Allowed mud levels to settle." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 299m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: POOH with cement stinger on 5' DP from 1928 m to 299 m MD. Stopped filling well on 2 last stands of 5' DP in order to allow mud column to drop for forthcomming repair of diverter seals. Trip speed 930 m/hrs." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 299m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Held toolbox talk. Changed from 5' to 3 1/2' handling equipment." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: POOH with cement stinger on 3 1/2' DP. Laid out 3 1/2' DP singles. Trip speed 150 m/hrs." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cleared and tidied drillfloor." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 0.2 hours. Operational details: Waited on cement. Meanwhile held toolbox talk for removal of diverter." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 0.5 hours. Operational details: Waited on cement. Meanwhile prepared for pulling diverter. Removed autoslips from RT. Picked up diverter pullling tool. Prepared diverter inserts." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 1.5 hours. Operational details: Waited on cement. Meanwhile disengaged diverter overshot mechanical seal. Installed 18 inch and 10 inch inserts in diverter. Engaged pulling tool and pulled diveter." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 1.5 hours. Operational details: Waited on cement. Meanwhile laid down diverter horizontally." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 1.5 hours. Operational details: Waited on cement. Meanwhile changed primary seal in diverter overshot." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 4.0 hours. Operational details: Changed primary seal in diverter overshot. Meanwhile waited on cement." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.8 hours. Operational details: Changed primary seal in diverter overshot. Meanwhile performed test against cement plug : Closed shear ram. Topped up well with mud by circulating accross choke and kill lines. Perfomed line test against kill valve on BOP - 200 bar / 5 min - ok. Opened kill valve. Pressured up on well against cement plug to 50 bar and observed steady test. Continued pressuring up in 20 bar increments, observed steady test on each level. Tested cement plug #2 to 162 bar / 10 min (0,74 % drop). Pumped and bled back 1022 litres. Meanwhile changed primary seal in diverter overshot." "On 2008-12-04, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed primary seal in diverter overshot." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed primary seal in diverter overshot." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Picked up diverter. Removed outer ring and automatic slips from RT. Landed diverter. Removed diverter running tool. Removed diverter inserts." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed outer ring and automatic slips in RT. Laid out diverter running tool. Cleaned and tidied drillfloor." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up 9 5/8' EZSV." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Picked up and made up EZSV running tool to stand of 5 1/2' DP. Made up 9 5/8' EZSV to running tool." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 610m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.2 hours. Operational details: RIH with 9 5/8' EZSV on 5 1/2' DP from surface to 610 m MD. Tripping speed 271 m/hrs." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 800m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIH with 9 5/8' EZSV from 610 m to 800 m MD. Tripping speed 190 m/hrs." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 800m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1416m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: RIH with 9 5/8' EZSV from 800 m to 1416 m MD. Tripping speed 410 m/hrs." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1437m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: Made up TDS to stand of 5 1/2' DP. RIH to EZSV setting depth at 1437 m MD. Attempted to wash across setting area at 70 lpm, but unable to maintain flowrate due to increasing SPP (22 bar max). Took up/down weights 115/103 MT, neutral 109 MT." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1437m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Set EZSV at 1437 m MD by applying 35 righthand rotations / torque 2-4 kNm. Picked up weight and sheared setting sleeve with 26 MT overpull. Picked up 3 m above plug and ran back in to 1437 m MD and tagged plug with 10 MT set down - ok." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1432m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: Pulled back to 1432 m MD. Displaced well from 1,34 sg to 1,44 sg OBM at 2900 lpm / SPP 100 bar. Flowchceked well for 10 min - well static." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1432m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 5 m3 1,77 sg slug and chased to drillfloor. Allow mud level to settle." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH with EZSV setting tool from 1432 m MD to surface. Tripping speed 954 m/hrs." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Removed autoslips and laid out EZSV setting tool." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up WBRRT/ jetting sub to stand of 5 1/2' DP." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with WBRRT/jetting sub to 139 m MD on 5 1/2' DP. Jetted accross wellhead at 3100 lpm / SPP 34 bar / 5 rpm. Set WBRRT in wearbushing." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Attempted to pressure test BOP. Observed rapid leak off at 20 bar. Attempted to seat WBRRT twice and re-test - negative. Observed mud return in pipe indicating leakage accross WBRRT." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Released WBRRT from wearbsuhing. POOH from 139 m MD to surface. Reset WBRRT according to Vetco instructions." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for running 18 3/4' BOP test plug." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up 18 3/4' BOP test plug. RIH with test plug on 5 1/2' DP from surface to 139 m MD. Seated test plug in wearbushing." "On 2008-12-05, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop activities' and lasted for 6.0 hours. Operational details: Pressure tested BOP and IBOPs to 20/345 bar 5/10 min." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Removed IBOP test swadge from TDS." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH with 18 3/4' BOP test plug from 139 m MD to surface. Broke and laid down testplug." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up WBRRT. RIH with WBRRT on 5 1/2' DP from surface to 139 m MD." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made several attempts to engage WB with pulling tool - set down 5-10 MT - no overpull observed. Landed 20-30 cm shallow relative to planned tally and WH datum. Decided to pull tool for inspection." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with WBRRT from 139 m MD to surface. No wear bushing retrieved." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Inspected WBRRT tool. Inspected and checked verified correct dies. Function tested tool in rotary - ok. Measured WBBRT - correct lenght." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with WBRRT on 5 1/2 DP. Measured DP on way in to verify correct lenght." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made several attempts to engage wearbushing. Verified measurments and found that WBRRT was landed 20 cm shallow relative to datum when setting down 10 MT." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Circulated accross WH/wearbushing at 3000 lpm / SPP 10 bar. Pumped a total of 28 m3." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Made several attempts to engage wearbushing - negative. Not able to enter and engage tool in wearbushing. Discussed situation - decided to pull WBRRT for changing to back up tool and HWDP." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with WBRRT on 5 1/2' DP from 139 m MD to surface. No wearbushing retrieved." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Broke and laid out WBRRT." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Brought back-up WBRRT to drillfloor. Made up WBRRT to stand of 5 1/2' HWDP" "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 112m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: RIH with WBRRT on 5 1/2' HWDP from surface to 112 m MD. Observed HWDP slipping in PRS. Halted operation for changing dies in PRS." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 112m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Changed dies in aft PRS gripper head." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with WBRRT on 5 1/2' HWDP from 112 m to 139 m MD. Made up TDS to DP. Set down 6 MT on wearbushing. Pulled wearbushing free with 26 MT overpull." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with WB/WBRRT from 139 m MD to surface. Broke and laid down wearbushing and WBRRT. Cleaned and tidied drillfloor." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up MS seal retrieval tool. Made up jet sub to tool. Checked tool according to Vetco procedure." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with MS seal retrieval tool on 5 1/2' DP from surface to 139 m MD. Set down 6 MT on MS seal. Rotated and observed torque increase as prescribed. Shut in annular and pulled MS sea above wellhead. No significant overpull observed." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH with MS seal retrieveal tool on 5 1/2' DP from 139 m MD to surface. No MS seal recovered." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Reset MS seal retrieveal tool. RIH with MS seal retrieval tool on 5 1/2' HWDP from surface to 139 m MD. Jetted accross wellhead at 1700 lpm / SPP 18 bar / 5 rpm." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Engaged tool in MS seal and attempted to latch - set down up to 12 MT and rotated according to Vetco instructions. Closed annular and picked up above wellhead - no significant overpull observed. Repeated procedure twice - negative. Discussed options for pulling MS seal." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up from cement unit to BOP. Closed annular preventer. Pressurised annulus to 70 bar. Set down weight on MS seal and latched same. Pulled MS seal free with 30 MT overpull and picked up above wellhead. Opened annular and observed 900 litres drop in triptank indicating seal release. Monitored trip tank - well static." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with MS seal retrieval tool on 5 1/2' HWDP from 139 m MD to surface." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Laid out MS seal, retrieval tool and jet sub. Reset running tool. Observed hydraulic leak from PRS." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Repaired hydraulic leakage on PRS hose fitting." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up WBRRT to stand of 5 1/2' DP. Made up wearbushing w/o D-ring to running tool." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with WB/WBRRT on 5 1/2' DP from surface to 139 m MD. Set wearbushing in 10 3/4' casing hanger." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with WBRRT on 5 1/2' DP from 139 m MD to surface. Broke and laid down WBRRT." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Brought Smith 9 5/8' casing cutter from maindeck to catwalk. Picked up cutter assy in rotaary. Broke and laid down handling sub. Changed X-over on cutter assy. Function tested cutters according to Smith instructions. Secured cutters with wire and duct tape." "On 2008-12-06, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1250m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: RIH with 9 5/8' casing cutter on 5 1/2 DP from surface to 1250 m MD. Filled pipe with 1,44 OBM every 500 m. Tripping speed 625 m/hrs." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH with 9 5/8' casing cutter on 5 1/2 DP from 1250 m MD to 1422 m MD. Filled pipe with 1,44 OBM every 500 m. Tripping speed 688 m/hrs." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Made up TDP to drillstring. Loacted cutter at planned depth of 1422 m MD. Took up/down weights 100/96 MT. Recorded free rotating torque 4 kNm." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Filled pipe pumping at 500 lpm. Obtained pump benchmark for cutting casing 500 lpm / SPP 59 bar, stopped pumps. Started rotation with 120 rpm. Started circulation at 500 lpm. Observer torque bulidingup to 5-11 kNm indicating effective cutting. Noticed small shock in derrick after 2,5 min of cutting indicating successful cut. Stopped rotation. Increased pump rate to 900 lpm / 55 bar - good indication. Picked up 2,5 m above cut. Came down while pumping at 400 lpm, observed sudden pressure drop as prescribed when passing cut at 1422 m MD. Stopped pumping. Marked pipe and tagged top of cut casing 0,25 m below (cut gap)." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Closed annular and lined up to choke. Observed for pressure bulid up for 10 min - none observed. Opened annular and flowcecked well for 15 min - well static." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1422m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Pumped 3 m3 1,67 sg slug. Allowed mud levels to settle." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: POOH with 9 5/8' casing cutter on 5 1/2' DP from 1422 m MD to surface. Tripping speed 711 m/hrs." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Removed autoslips from rotary. Installed masterbushing and bowls. Broke out Smith 9 5/8' casing cutter. Installed handling sub and laid out assy." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and tidied drillfloor for safety." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Held toolbox talk for picking up 10 3/4' bowen spear." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Picked up and hung off packoff tool. Picked up and made up 10 3/4' Bowen spear and bumper sub. Set grapple to catch and secured same with duct tape." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 15m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Changed die carriers and dies in IR." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 25m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Changed dies in IR. Picked up and made up single 8 1/4' DC." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 25m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 129m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: RIH with 10 3/4' Bowen spear on 8 1/4' DC / 5 1/2' HWDP from 25 m to 129 m MD." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 153m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Made up TDS to 5 1/2' HWDP. RIH to 153 m MD and landed stop ring in 10 3/4' wearbushing at 140 m MD. Engaged spear in 10 3/4' casing according to Smith instructions." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1420m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Released casing with 168 MT weight. Picked up 2 m and confirmed 9 5/8' casing free." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1420m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.2 hours. Operational details: Staged up pumps to 2000 lpm / SPP 24-28 bar and circulated annulus clean. Observed little solids on shakers and good condition of mud returns. Circulated 1,5 times bottoms up." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1420m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Held toolbox talk for pulling 9 5/8' casing. Had problem with PRS flush joint elevator." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1420m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Troubleshot problem with PRS elevator." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1305m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: POOH with 9 5/8' casing on spear/landing string from 1420 m to 1305 m MD." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1305m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Installed 6 3/8' reg x 5 1/2' VemEIS x-over on last 8 1/4' DC in landing string. Installed 5 1/2' HWDP single for racking purposes. Pulled 10 3/4' casing hanger to surface and hung off in RT on 9 5/8' pup joint." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1277m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Released 10 3/4' Bowen spear and pulled out of casing. Removed wearbushing using slings and tugger. Re-engaged spear in 10 3/4' casing hanger. Picked up 3 m and hung off casing hanger on 1st full 9 5/8' casing joint, i.e. approx 5 m stick-up." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1277m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: Disengaged spear, removed and suspended in PRS. Rigged up Odfjell casing tong. Prepared PS-30 slips." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1277m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Slung up 10 3/4' casing hanger assy. Broke casing connection and laid down hanger assy using tugger. Changed to 9 5/8' segment in BX elevator." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1277m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Made up 9 5/8' swadge to 9 5/8' casing. Pumped 5 m3 1,67 sg slug and chased to drillfloor. Broke swadge." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1277m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Removed masterbushing and installed PS-30 in RT." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1121m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.0 hours. Operational details: POOH with 9 5/8' 53,5# C95 casing from 1277 m to 1121 m MD. Pulling speed 7 jnts/hr. Had problems with HTS tailing arm and casing tong." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1121m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot hydraulics for casing tong. Troubleshot HTS tailing arm." "On 2008-12-07, at Well NO 15/9-F-15, a drilling event occurred at a depth of 707m. The activity was categorized as 'plug abandon -- cut' and lasted for 3.0 hours. Operational details: POOH with 9 5/8' 53,5# C95 casing from 1121 m to 707 m MD. Breakout torque in 30 000 ft lbs range. Pulling speed 11 jts/hr." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 4.2 hours. Operational details: POOH with 9 5/8' 53,5# C95 casing from 707 m MD to surface. Pulling speed 14 jts/hr." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Laid down cut 9 5/8' casing joint. Cleaned and tidied drillfloor. Removed 9 5/8' elevator inserts. Rigged down and removed Odfjell casing tong. Removed PS-30 slips from RT." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed masterbushing, bowl and hole cover. Removed casing running equipment from drillfloor." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Broke and laid out 5 1/2' HWDP and 8 1/4' DC. Broke and laid down 10 3/4' Bowen spear and pack off assy. Changed dies in PRS." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Picked up and made up WBRRT. Made up nominal seat protector. RIH with WBRRT/NSP on 5 1/2' DP from surface to 139 m MD. Set nominal seal protector in wellhead." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH with WBRRT from 139 m MD to surface. Reset WBRRT, broke and laid out same." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for running cement string." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Changed from 5 1/2' to 5' handling gear." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 325m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH on 5' DP from surface to 325 m MD." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 325m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Changed from 5' to 5 1/2' handling gear." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1363m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.8 hours. Operational details: RIH on 5 1/2' DP from 325 m to 1363 m MD." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1363m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Laid out single from 5 1/2' stand for space out purposes. Made up TDS to string. Broke circulation and staged up pumps to 2500 lpm / SPP 45 bar. Washed down from 1363 m to 1422 m MD. Hung up on cut casing at 1422 m MD and observed SPP increasing to 75 bar. Picked up and started rotation at 10 rpm." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1435m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Passed cut at 1422 m, RIH and tagged EZSV at 1435 m MD. Picked up 1 m to 1434 mMD. Circulated and condtioned mud at 2500 lpm / SPP 46 bar / 85 RPM / 3-8 kNm." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1434m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Lined up cement unit and performed line test to 200 bar / 5 min - ok. Pumped 16 m3 og 1,7 sg cement spacer using rigpumps at 2000 lpm / SPP 30 bar. Chased spacer with 2,6 m3 OBM to fill standpipes." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1434m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pumped 22,9 m3 2,0 sg cement at 800 lpm. After 14 m3 pumped, picked up 1 m to 1433 m MD. Chased cement slurry to drillfloor with 890 liters of water. Theoretical top of cement at 1318 m MD." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1434m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Using rig pumps ; displaced cement with 12,3 m3 OBM to give 1 m3 underdisplacement in string. Pump rate 2000 lpm slowing down to 500 lpm at the end of the displacement. Observed no pressure bulid up during displacement." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1238m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Pulled 5 stands of dry pipe from 1434 m to 1238 m MD. Pulling speed 6 min/std." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1238m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.0 hours. Operational details: Inserted 2 ea sponge balls for cleaning string. Stepped up pumps to 2500 lpm / SPP 42 bar and rotated at 120 RPM. Circulated out excess spacer and cement. Sampled mud and routed contaminated returns to separate pit. No visual observation of cement returns." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1198m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH with 1 stand wet. Pumped 5m3 1,67 sg slug. Allowed mud levels to settle." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 325m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: POOH with 5 1/2' DP from 1198 m to 325 m MD. Tripping speed 700 m/hrs." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 325m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Changed from 5 1/2' to 5' handling gear." "On 2008-12-08, at Well NO 15/9-F-15, a drilling event occurred at a depth of 90m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH with 5' DP from 325 m to 90 m MD. Tripping speed 470 m/hrs." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH with 5' DP from 90 m MD to surface." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- wait' and lasted for 4.2 hours. Operational details: Waited on cement to set up. Meanwhile tested FOSV. Re-arranged stands of 9 5/8' casing racked back in derrick. Moved stands to aft setback area, doped box end of stands." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up 17 1/2' drilling BHA." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Picked up and hung of 17 1/2' powerdrive. Picked up and made up powerpulse HF. Picked up and made up ARC-9. Picked up and made up 9 5/8' NMDC single." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Picked up and made up 9 1/2' NMDC. Picked up and and made up 7 5/8' reg x 6 5/8' reg box crossover." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 43m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk / handover meeting." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- trip' and lasted for 3.2 hours. Operational details: Continued to make up 17 1/2' drilling BHA. Had problems to access fingerboard with PRS due to conflict with dual latch bracket. Set ZMS in override and ran PRS manually. Made up and ran stand with jar and 8 1/4' DC. Made up and ran stand with accelerator and 8 1/4' DC. Installed totco ring. Made up 6 5/8' reg x 5 1/2 FH box crossover. Had problems with PRS when attempting to pick up stand of 5 1/2' HWDP." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 108m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Troubleshot PRS weight indicator and PRS elevator problems." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Made up stand of 5 1/2' HWDP. Removed masterbushing. Installed autoslips in RT. RIH with 17 1/2' BHA on 5 1/2' DP to 147 m MD. Prevailing problems with PRS when attempting to pick up stands of 5 1/2' HWDP." "On 2008-12-09, at Well NO 15/9-F-15, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 11.5 hours. Operational details: Troubleshot situation with PRS. PRS not supplying sufficient hydraulic pressure to gripper claw. Performed faultfinding in hydraulic and electrical system." "On 2008-12-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 6.0 hours. Operational details: Perfomed faultfinding in PRS hydraulic and electrical system. Meanwhile installed pump in sub on drillstring and circulated in well at 2300 lpm to power down MWD batteries. Performed cleaning and general PM in drilling areas." "On 2008-12-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 228m. The activity was categorized as 'interruption -- other' and lasted for 13.0 hours. Operational details: Troubleshot problems with aft PRS. Found fault to be in control system, not supplying enable signal to solenoid valve which regulates the hydraulic pressure to the gripper claw. Meanwhile perfomed cleaning and general PM in drilling areas." "On 2008-12-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 228m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Cleared drillfloor. Installed flush joint elevator on PRS. Tested PRS - ok." "On 2008-12-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 228m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Calibrated blocks -ok." "On 2008-12-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 228m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Rigged down cement hose and pump in sub." "On 2008-12-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 228m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Removed masterbushing. Installed PS-30 in rotary." "On 2008-12-10, at Well NO 15/9-F-15, a drilling event occurred at a depth of 228m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to RIH with 17 1/2' drilling BHA." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1074m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP from 228 m to 1174 m MD. Tripping speed 370 m/hrs." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1074m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Filled drillsting pumping at 500 lpm." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1074m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Performed choke drill." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1235m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP from 1074 m to 1235 m MD. Made up TDS to drillstring." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1301m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Washed from 1235 m to 1301 m MD. Parameters : 2000 lpm / 30 RPM / SPP 60 bar / Torque 4-5 kNm / WOB < 1 MT." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1315m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Washed/drilled soft cement from 1301 m to 1315 m MD. Parameters : 2000 lpm / 30 rpm / SPP 60 bar / torque 5-15 kNm / WOB 0-5 MT." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1318m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Increased pump rate to 4000 lpm. Washed/drilled down to 1318 m MD and tagged hard cement. Parameters : 4000 lpm / 210 bar SPP / 30-50 rpm / torque 5-13 kNm / WOB 3-8 MT." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1368m. The activity was categorized as 'plug abandon -- mill' and lasted for 4.5 hours. Operational details: Drilled cement in 20' casing from 1318 m to 20' shoe depth at 1368 m MD. Drilling parameters : 4000 lpm / SPP 193-205 bar / ECD 1,43-1,46 / 5-8 MT WOB / 60 RPM / Torque 6-12 kNm." "On 2008-12-11, at Well NO 15/9-F-15, a drilling event occurred at a depth of 1378m. The activity was categorized as 'plug abandon -- mill' and lasted for 4.5 hours. Operational details: Drilled cement below 20' shoe and new formation from 1368 m to 1381 m MD. Encountered soft cement underneath shoe. Initiated kick-off. Drilling parameters : 4000 lpm / SPP 190 bar / ECD 1,43-1,44 / 1-2 MT WOB / 60 RPM / Torque 6-10 kNm. ****Operations transferred to F-15****" "On 1992-09-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 3.0 hours. Operational details: PULLED AND BOLSTERED ANCHORS NO.5, 1 AND 8" "On 1992-09-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 3.0 hours. Operational details: WAITING ON NPD APPROVAL TO MOVE THE RIG. CONTINUE WORKING ON OUT- STANDING ITEMS ACCORDING TO PUNCHLISTS." "On 1992-09-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 3.0 hours. Operational details: CONTINUE WAITING ON NPD APPROVAL TO MOVE THE RIG." "On 1992-09-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 3.0 hours. Operational details: PULLED AND BOLSTERED ANCHORS NO.3 AND 7. BEGIN PULLING ANCHOR NO. 6" "On 1992-09-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 8.0 hours. Operational details: PULLED AND BOLSTERED ANCHOR NO 6." "On 1992-09-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 10.0 hours. Operational details: WAITED ON NPD APPROVAL TO MOVE RIG. WORKED ON OUTSTANDING ITEMS ON PUNCH LIST." "On 1992-09-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 6.0 hours. Operational details: CONTINUED WAITING ON APPROVAL TO MOVE RIG. WORKED ON OUTSTANDING ITEMS ON PUNCH LIST. M/U FRAMO UMBILICAL TO CTS FOR FUNCTION TEST." "On 1992-09-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 7.0 hours. Operational details: WAITING ON APPROVAL TO MOVE RIG. WORKED ON OUTSTANDING ITEMS ON PUNCH LIST. FUNCTION TESTED FRAMO CTS." "On 1992-09-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.0 hours. Operational details: PULLED AND BOLSTERED ANCHOR NO 2." "On 1992-09-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 10.0 hours. Operational details: RIG ON MOVE TO LOCATION 15/9-C" "On 1992-09-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 6.0 hours. Operational details: RIG ON MOVE." "On 1992-09-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 18.0 hours. Operational details: RIG ON MOVE TO LOCATION 15/9-C" "On 1992-09-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 6.0 hours. Operational details: RIG ON MOVE TO LOCATION 15/9-C" "On 1992-09-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 18.0 hours. Operational details: RIG ON MOVE TO LOCATION 15/9-C" "On 1992-09-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 6.0 hours. Operational details: RIG ON MOVE TO LOCATION 15/9-C" "On 1992-09-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 18.0 hours. Operational details: RIG ON MOVE TO LOCATION 15/9-C" "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 3.0 hours. Operational details: RIG ON MOVE TO LOCATION 15/9-C" "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.0 hours. Operational details: DROPPED ANCHOR NO 7, ON BOTTOM 03:00 HRS. CHECKED ANCHOR HOLDING 50 TON, OK." "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 0.5 hours. Operational details: UNLOADED NORDMANN BORG." "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.5 hours. Operational details: MOVED RIG TO TEMPLATE,PREPARED TO RUN ROV." "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 2.0 hours. Operational details: JUMPED ROV.INSPECTED TEMPLATE AND INSTALLED HONEYWELL TRANSPONDER IN A1. UNABLE TO DISCONNECT TRANSPONDER DUE TO LIGHT FAILURE ON ROV. PULL ROV AND TRANSPONDER." "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 6.5 hours. Operational details: ANCHOR ON BTM LENGTH BOAT ANCHOR ON BTM LENGTH BOAT NO.2 09:15 1012M MEARSK SUPPORT NO.3 09:22 1312M NORMAND BORG NO.1 10:30 1129M NORMAND BORG NO.6 11:06 1098M SOLFONN NO.5 13:02 1220M SOLFONN NO.4 14:15 1242M SOLFONN" "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 3.0 hours. Operational details: JUMPED ROV AND INSPECTED TEMPLATE. POS. RIG AND INSTALLED HONYWELL TRANSPONDER IN PILE SLEEVE A1. RETRIVED SIMRAD HPR TRANSPONDER IN C1. LOST TRANSPONDER ON WAY OUT. LOCATED TRANSPONDER W/ROV ON SEA BED 10-15M FROM S3 ON TEMPLATE." "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 2.5 hours. Operational details: SET OUT ANCHOR NO.8 W/NORMAND BORG. ON BTM. AT 20:05 HRS. LENGTH 1059M" "On 1992-09-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 4.0 hours. Operational details: DEBALLASTED RIG TO OPERATION DRAFT." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 1.0 hours. Operational details: CONTINUE DEBALLASTED RIG." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 2.0 hours. Operational details: ATTEMTED TO SET OUT CTS ANCHOR. WIRE FROM RIG TO NORMAND BORG WAS ACRO SS EMERGENCY TOWING LINE." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.0 hours. Operational details: REARRANGED WIRE FROM RIG TO NORMAND BORG." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.5 hours. Operational details: PULLED CTS ANCHOR OVER TO NORMAND BORG. REARRANGED CTS ANCHOR." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 0.5 hours. Operational details: POSISTIONED NORMAND BORG AND DROPPED CTS ANCHOR 120M/110 DEG. FROM TEMPLATE." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: INSPECTED CTS ANCHOR WITH ROV. RELEASED ROV HOOK. PULLED HOOK TO NORMAND BORG." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: JUMPED SEA OWL,RETRIEVED SAME DUE TO ELECTRICAL FAILURE." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 4.5 hours. Operational details: PULLTESTED ANCHORS TO 160 TON,OK. JUMPED SEA OWL. POSITIONED RIG OVER TEMPLATE." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: PREPARED GUIDE LINE NO.4 TO OPEN HATCH,WHILE PERFORMED TEMPLATE SURVEY W/ROV." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: OPENED LATCH ON HATCH S3. ESTABLISHED WIRE TO OPEN HATCH. OPENED HATCH S3. INSPECTED HINGES,RELEASED WIRE. STABBED AND INSTALLED GUIDE WIRE NO.4. PULLTESTED SAME TO 2 TON,OK." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: INSTALLED GUIDE WIRE NO.1 AND PULLTESTED SAME WITH 2 TON,OK." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: MOVED RIG 12M IN DIR. 110 DEG. OPERATION INTERRUPTED DUE TO PROBLEMS ON GUIDE LINE NO.4." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: INSTALLED GUIDE WIRE NO.2 AND NO.3 PULLTESTED SAME TO 2 TON. MOVED RIG 25M FROM TEMPLATE IN DIR. 110 DEG." "On 1992-09-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: P/U 5' HWDP" "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: CONT. P/U 5' HWDP AND RACKED SAME BACK IN DERRICK. M/U 26' BIT FOR RUNNING CTS." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: PICK UP 9 1/2' DRILL COLLARS." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: MADE UP SPUD ASSEMBLY." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: DRIFTED CTS TO 34' USING 34'/36' HOLEOPENER." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: BREAK CONNECTION BWETWEEN FRONT DRILL AND HOLE OPENER. TREADS DAMAGE. LAID DOWN BOTH." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: MADE UP 1 STAND 9 1/2' DC AND RACKED BACK IN DERRICK." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: STABBED INTO CTS PUMP UNIT WITH 26' BIT. CLOSED RAM AND PERFORMED PICK UP TEST." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: PREPERED CTS PUMP AND HOSE FOR RUNNING." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: PICKED UP AND RAN CTS PUMP AND HOSE." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: HOOKED UP COOLING TO CTS FROM RIG SYSTEM." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: RAN CTS TO 78M." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: WIRE CONNECTED TO MIDDLE POINT OF CTS HOSE TO SHORT. CLAMPED ON NEW WIRE." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RAN CTS." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CHECKED WIRE/HOSES WITH ROV." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POSITIONED RIG OVER WELL. CHECKED WIRE/HOSES WITH ROV." "On 1992-09-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: RAN CTS. CHECKED WIRE/HOSES WITH ROV." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: RAN CTS. HAD PROBLEMS STABBING INTO PGB AND USED SCORPION TO HELP STABBING. STABBED IN WITH CTS 01:40 HRS." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: TOOK WEIGHT WHEN CTS WAS 1.20M ABOVE PGB. CHECKED CTS HOSE, HYDRAULIC HOSE, OK. SLACKED OFF CTS WEIGHT (5-6 TONS). CTS STILL AT THE SAME PLACE." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: STARTED CTS PUMP. MAX. RATE APPROX. 7000 L/MIN. WITH 160 BAR PRESSURE, WHILE OBSERVING OUTLET CTS HOSE WITH ROV." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: SET BIT ON BOTTOM AT 108,5M. JETTED FROM 108,5M TO 110M. MAX RATE 1650 L/MIN. CTS PUMP LANDED ON PGB." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: OPENED RAM ON CTS. PULLED 26' BIT ABOVE TEMPLATE." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: MOVED RIG 25M, DIRECTION 110 DEG.." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: PULLED OUT OF HOLE WITH CTS LANDING STRING." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: PULLED OUT OF HOLE WITH CTS LANDING STRING. LAID DOWN BIT AND SUBS." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 7.0 hours. Operational details: MADE UP AND RACKED BACK 10 STANDS 5' DP." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: PICKED UP BOTTOM HOLE ASSEMBLY NO.1. SET MEMORY ON MWD AND FUNCTIONED SAME, OK." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: MADE UP JAR, 2 X 8' DC, CROSSED OVER TO HWDP AND RAN IN TO 91M." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: MOVED RIG TO 15M OFF LOCATION." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: INSTALLED AND RAN GUIDE FRAME. FOUND WIRE FOR CTS HOSE TWISTED. UNTWISTED SAME." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: MOVED RIG IN POSITION OVER TEMPLATE." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: UNTWISTED WIRE FOR CTS HOSE." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: HELD SHALLOW GAS MEETING WITH THE CREW." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: STAB INTO CTS PUMP AT 2315 HRS. RIH TO 107M. PULLED GUIDE FRAME TO SURFACE." "On 1992-09-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CLOSED RAM ON CTS PUMP AND TOOK SURVEY WITH MWD TOOL. INSPECTED CTS HOSE." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POSITIONED RIG. TOOK SURVEY ON BOTTOM 0,3 DEG." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: INSPECTED CTS HOSE WITH ROV AND STRAIGHTED SAME." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 134m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: DRILLED 9 7/8' PILOTHOLE FROM 109 M TO 134 M." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 107m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: SWEEPED HOLE WITH 5 M3 HI-VIS MUD. POOH TO CTS PUMP, DUE TO FAILURE ON DEPTH SENSOR TO MWD." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: RIH TO 134 M. DRILLED 9 7/8' PILOTHOLE FROM 134 M TO 180 M. PUMPED 5 M3 HI-VIS MUD ON EVERY STAND." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 195m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED 9 7/8' PILOTHOLE FROM 180 M TO 195 M." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: HELD SHALLOW GAS MEETING WITH CREW." "On 1992-09-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 547m. The activity was categorized as 'drilling -- drill' and lasted for 17.0 hours. Operational details: DRILLED 9 7/8' PILOTHOLE FROM 195 M TO 547 M. PUMPED 5 M3 HI-VIS PILL ON EVERY CONNECTION." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 547m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: PUMPED 10 M3 HI-VIS PILL FOLLOWED BY 10 M3 SEAWATER AND 10 M3 1,25 SG HI-VIS MUD." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH TO 15 M ABOVE TEMPLATE. PUMPED 0,7 M3 1,25 SG HI-VIS MUD ON EVERY STAND WHEN PULLING OUT." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: PULLED RIG 35 M DIRECTION 110 DEG." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH. L/D 8' MWD." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: M/U 12 1/4' BIT,34'/36' HOLEOPENER, REARRANGED BHA AND RIH TO 92 M." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 92m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POSITIONED RIG OVER TEMPLATE" "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 128m. The activity was categorized as 'drilling -- hole open' and lasted for 3.5 hours. Operational details: STABBED INTO CTS PUMP,CLOSED CTS RAM TO CENTER STRING. OPENED UP 9 7/8' PILOT HOLE TO 36' FROM 109 M TO 128 M." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: REPAIRED SPEED CONTROL ON DRAW WORK." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 147m. The activity was categorized as 'drilling -- hole open' and lasted for 1.5 hours. Operational details: OPENED UP 9 7/8' PILOTHOLE TO 36' FROM 128 M TO 147 M." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: INVESTIGATED FAILURE ON DRAW WORK SPEED CONTROL SYSTEM." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- hole open' and lasted for 1.5 hours. Operational details: OPENED 9 7/8' PILOTHOLE TO 36' FROM 147 M TO 170 M. (12 1/4' BIT AT 172 M)" "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: DISPLACED HOLE WITH 40 M3 HI-VIS MUD." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: DROPPED SINGLE SHOT SURVEY, PULLED STRING TO 118 M, RETRIEVED SURVEY WITH SLICK LINE. RIH TO 170 M. (SURVEY 'BULLSEYE')" "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: DISPLACED HOLE WITH 90 M3 1,25 SG HI-VIS MUD." "On 1992-09-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH TO 118 M, CLOSED CTS RAM,PULLED CTS PUMP ON 34'/36' HOLEOPENER TO ABOVE TEMPLATE." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: PULLED RIG 25 M DIRECTION 110 DEG." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH WITH BHA AND CTS PUMP.OUT OFF WATER 03:00 HRS." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: SECURED CTS PUMP ON TROLLEY,OPENED CTS RAM,PULLED 34'/36' HOLEOPENER RACKED SAME IN DERRICK." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: PREPARED FOR RUNNING 30' CASING, PICKED UP SHOE AND CHECKED SAME." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 91m. The activity was categorized as 'drilling -- casing' and lasted for 6.5 hours. Operational details: RAN 30' CASING TO 91 M." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POSITIONED RIG OVER TEMPLATE." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 166m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: STABBED 30' INTO PGB, LANDED 30' CASING. SHOE AT 166 M. CHECKED LOCKRING ENGAGED WITH 22 TON OVERPULL, OK." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 166m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: HOOKED UP CEMENT HOSE.PRESSURE TESTED SURFACE LINES TO 100 BAR,OK. CIRCULATED 19 M3 WITH SEAWATER.STARTED TO MIX AND PUMP CEMENT." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 166m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: LOST MIXWATER INTO SEA THROUGH TRIPTANK, FOUND ONE VALVE OPEN. CIRCULATED OUT CEMENT, MADE NEW LEAD MIXWATER IN PIT." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 166m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: MIXED AND PUMPED 17,2 M3 1,56 SG LEAD SLURRY, FOLLOWED BY 15 M3 1,9 SG TAIL SLURRY, DISPLACED SAME WITH 4,6 M3 SEAWATER. FLOWCHECKED-OK." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: B/U 30' RUNNING TOOL , TESTED SCR'S WHILE CLEANED PIPE. PULL STINGER ABOVE TEMPLATE." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PULLED RIG 25 M DIRECTION 110 DEG." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: POOH, L/D 30' RUNNING TOOL." "On 1992-09-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: DISCONNECTED CTS EXTENSION PIPE FOR 36' HOLE." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: M/U CTS EXTENSION FOR DRILLING 26' HOLE." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: M/U 18 3/4' HOUSING JOINT, RACKED SAME IN DERRICK." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: M/U 26' BHA." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 44m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: M/U 26' BHA, TESTED MWD OK.CLOSED CTS RAM ON 26' HOLEOPENER. RIH WITH CTS PUMP/26' HOLEOPENER TO 44 M." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 44m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: SORTED OUT LOOP ON CTS HOSE." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 72m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH WITH CTS PUMP/26' HOLEOPENER TO 72 M." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 72m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: POSITIONED RIG OVER TEMPLATE." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 162m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: LANDED CTS PUMP ON 30' HOUSING,CONTINUED RIH WITH 12 1/4' BIT/26' HO. TAGGED CEMENT AT 162 M." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: SORTED OUT LOOP ON CTS HOSE." "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: DRILLED CEMENT FROM 162 M,30' SHOE AT 166 M AND CEMENT TO 170 M. (12 1/4' BIT AT 172 M)" "On 1992-09-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 230m. The activity was categorized as 'drilling -- hole open' and lasted for 5.0 hours. Operational details: OPENED 9 7/8' PILOTHOLE TO 26' HOLE FROM 170 M TO 230 M. PUMPED 5 M3 HI-VIS PILL EVERY 15 M DRILLED." "On 1992-09-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 311m. The activity was categorized as 'drilling -- hole open' and lasted for 6.0 hours. Operational details: OPENED 9 7/8' PILOTHOLE TO 26' FROM 230 M TO 311 M. PUMPED 5 M3 HI-VIS PILL ON EVERY 15 M DRILLED." "On 1992-09-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- hole open' and lasted for 15.0 hours. Operational details: OPENED 9 7/8' PILOTHOLE TO 26' HOLE FROM 311 M TO 545 M. (12 1/4' BIT AT 547 M) PUMPED 5 M3 HI-VIS PILL ON EVERY 15 M DRILLED." "On 1992-09-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: PUMPED 10 M3 HI-VIS PILL,FOLLOWED BY 60 M3 OF SEAWATER.DISPLACED HOLE WITH 110 M3 HI-VIS PILL." "On 1992-09-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH TO 30' CASING SHOE. MAX OVERPULL 20 TON AT 420 M. RIH TO 545 M. WORKED TIGHT SPOT AT 420 M,OK." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: PUMPED 200 M3 OF SEAWATER FOLLOWED BY 45 M3 HI-VIS PILL. DISPLACED HOLE WITH 120 M3 1,25 SG HI-VIS MUD." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH TO 122 M,CLOSED CTS RAM,PULLED CTS PUMP/26' HOLEOPENER ABOVE TEMPLATE." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: MOVED RIG 25 M DIRECTION 110 DEG." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH WITH CTS PUMP/26' HOLEOPENER.SECURED CTS PUMP ON TROLLEY." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: SECURED CTS PUMP,OPENED CTS RAM,RACKED 26' HOLEOPENER BACK IN DERRICK." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 85m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: PREPARED AND RAN 20' CASING TO 84 M. LOCKED FIRST 3 JOINTS. M/U CEMENT HEAD ON DP,RACKED SAME IN DERRICK." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POSITIONED RIG OVER TEMPLATE." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 84m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: GUIDE WIRE NO.3 HOOKED ON 20' CASING,SORTED SAME OUT,OK." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 531m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: RAN 20' CASING,LATCHED ON 30' HOUSING,20' SHOE AT 531 M. TOOK 18 TON OVERPULL,OK." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 531m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: HOOKED UP SURFACE LINES, PUMPED 95 M3 SEAWATER.MAX 2000 L/MIN. PRESSURE TESTED SURFACE LINES TO 100 BAR,OK." "On 1992-09-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 531m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: MIXED AND PUMPED 101 M3 1,56 SG LEAD SLURRY,FOLLOWED BY 15 M3 1.9 SG TAIL SLURRY.RELEASED DART ,DISPLACED CEMENT W/74,1 M3 1,25 SG MUD. SHEARED WIPERPLUG W/345 BAR. BUMPED PLUG AND PRESSURE TESTED 20' CASING TO 70 BAR." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RELEASED 20' RUNNING TOOL BY 3 RIGHT HAND TURNS. PULLED RUNNING TOOL ABOVE TEMPLATE." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: MOVED RIG 25 M DIRECTION 110 DEG." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: L/D CEMENT HEAD,POOH L/D 20' RUNNING TOOL." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 82m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: M/U CORROSION CAP,RIH TO 82 M. INSTALLED MODIFIED GUIDE FRAME." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: WASHED WELLHEAD,USING SCORPION.PERFORMED SURVEY ON WELLHEAD,OK." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POSITIONED RIG OVER TEMPLATE." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: LANDED CORROTION CAP." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: MIXED AND PUMPED INHIBITOR.OBSERVED WITH ROV,OK. SHEARED PINS ON CORROTION CAP RUNNING TOOL WITH 5 TON OVERPULL. POOH TO 81 M." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.5 hours. Operational details: RELEASED AND PULLED 3 GUIDE LINE ANCHORS." "On 1992-09-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: HOOKED GUIDELINE ANHCOR NO.3 TO HATCH NO.3. CLOSED AND LOCKED SAME. (END OFF REPORT,CONT. ON REPORT NO.1 ON WELL 15/9-C 2H)" "On 1992-11-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 0.5 hours. Operational details: MOVED RIG 30M FORWARD" "On 1992-11-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: RELEASED BOP FROM CARRIER. LIFTED BOP OFF TEST STUMP. INSTALLED VX ON STUMP. SET BOP BACK ON TEST STUMP AND WELDED BOP TO CARRIER. REMOVED RISER AND MOVED CARRIER BACK FOR BOP TESTING." "On 1992-11-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: OPENED HATCH COVER ON SLOT NO. 3." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: INSTALLED GUIDE WIRES." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.0 hours. Operational details: MOVED RIG OVER WELL. PULL TESTED GUIDE LINES TO 2,5 TONS." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: RIH WITH CORROSION CAP R/R TOOL. RAN GUIDE FRAME. RETRIEVED CORROSION CAP WITH 15 TONS OVERPULL. POOH WITH CAP AND R/R TOOL." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: LD CORROSION CAP AND R/R TOOL." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 9.0 hours. Operational details: PRESSURE TESTED UAP TO 27/345 BAR, 5/15 MINS. PRESSURE TESTED LAP AND PIPE RAMS TO 27/690 BAR, 5/15 MINS." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 0.5 hours. Operational details: MOVED RIG 30 M OFF WELL." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: FOUND SHEAR RAM LEAKING. BROUGHT CARRIER UP IN HIGH POSITION. PREPARED FOR WORKING ON SHEAR RAM." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: SECURED BOP." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.5 hours. Operational details: FUNCTION TESTED BOP." "On 1992-11-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: WORKED ON SHEAR RAM." "On 1992-11-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: CONT. WORKING ON SHEAR RAM. FOUND T-SEAL TO BE DAMAGED." "On 1992-11-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: LD RISER AND RUNNING TOOL" "On 1992-11-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: CHANGED SAVER SUB IN TDS TO 6 5/8' FH." "On 1992-11-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: RU FOR AND CARRIED OUT TORQUE MEASUREMENTS FOR CALIBRATION PURPOSES." "On 1992-11-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: CONT.REPAIRING SHEAR RAM." "On 1992-11-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 17.0 hours. Operational details: W.O.W. TO RUN BOP/RISER" "On 1992-11-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONT W.O.W." "On 1992-11-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 10.5 hours. Operational details: CONT. WOW TO RUN BOP/RISER. WHILE WOW, REARRANGED 9 1/2' DC AND 8' DC IN DERRICK AND PU/MU 17 1/2' BHA AND RACKED SAME IN DERRICK." "On 1992-11-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: RD DRILLPIPE EQUIPMENT. RU TO RUN BOP. MOVED BOP/CARRIER IN PLACE. PU 2 EA 50 FT RISER JOINTS AND MU TO BOP. DEBALLASTED RIG, CUT BOP LOOSE FROM CARRIER AND BALLASTED RIG. INSTALLED GUIDE WIRES. LIFTED BOP OFF CARRIER, MOVED CARRIER AWAY AND RAN BOP THROUGH SPLASH ZONE. RU TO TEST K/C LINES. TESTED TO 30 BAR/5 MINS." "On 1992-11-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: ATTEMPTED PRESSURE TESTING K/C LINES TO 345 BAR, NEG. TEST PLUG LEAKING." "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: TESTED K/C LINES TO 345 BAR/10 MINS." "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.5 hours. Operational details: CONT. RUNNING BOP/RISER. PRESSURE TESTED K/C LINES TO 30/345 BAR, 5/10 MINS. MU SLIP JOINT AND HANDLING JOINT. MU GOOSE NECK FROM KILL LINE TO RISER. DE-BALLASTED RIG 2M." "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: CONT. INSTALLATION OF KILL/CHOKE LINES, RISER TENSIONERS AND SADDLE FOR POD HOSES. PRESSURE TESTED KILL/CHOKE LINES TO 35/345 BAR, 5/10 MINUTES." "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.0 hours. Operational details: POSITIONED RIG OVER WELL" "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 1.0 hours. Operational details: BALLASTED RIG TO DRILLING DRAFT" "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: LANDED BOP. OVERPULL TESTED WITH 25 TONS. CLOSED SHEAR RAM WITH ACOUSTIC SYSTEM AND PRESSURE TESTED 20' CASING AND SHEAR RAM TO 75 BAR/15 MINUTES. LAID DOWN LANDING JOINT. INSTALLED DIVERTER. RIGGED DOWN RISER HANDLING EQUIPMENT." "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.0 hours. Operational details: RIGGED UP PIPE HANDLING EQUIPMENT. MADE UP SPRING LOADED TOOL AND RAN IN HOLE. PRESSURE TESTED WELLHEAD CONNECTOR TO 20/345 BAR, 5/10 MINUTES. PULLED TOOL." "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: MADE UP SPRING LOADED TOOL TO 18 3/4' NOMINAL BORE PROTECTOR AND RAN IN HOLE. FUNCTION TESTED BOP ON BLUE POD FROM DRILLERS PANEL. RETRIEVED SPRING LOADED TOOL." "On 1992-11-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: INSTALLED SPIDER AND DIVERTER RUNNING TOOL. PICKED UP DIVERTER AND CHANGED OUT O-RINGS ON CONNECTION BETWEEN THE DIVERTER AND THE SLIP- JOINT INNER BARREL. RE-INSTALLED DIVERTER, OK." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 506m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: MADE UP BOTTOMHOLE ASSEMBLY NUMBER 4 AND RAN IN HOLE TO 506 METERS. TESTED MUD MOTOR AND MWD ON WAY IN." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 506m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: HELD KICK DRILL" "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 510m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONT. RUNNING IN TO DRILL FLOAT/CEMENT/SHOE" "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 525m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: TAGGED AT 517M. DRILLED PLUGS AND FLOAT FROM 517 TO 519 M AND CEMENT FROM 519 TO 525 M." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 525m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: ATTEMPTED TO TEST ACOUSTIC CONTROL SYSTEM, NEG. TROUBLE SHOOTING. RE-TESTED OK." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 531m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CONT. DRILLING CEMENT FROM 525 TO 531 M." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 531m. The activity was categorized as 'moving -- position' and lasted for 0.5 hours. Operational details: POSITIONED RIG" "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 547m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: DRILLED SHOE AT 531M. CLEANED OUT RAT HOLE TO 547M. PUMPED 35 M3 BENTONITE MUD." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 552m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: DISPLACED WELL TO 1,20 SG KCL MUD. DRILLED 5M NEW FORMATION FROM 547M TO 552M WHILE DISPLACING." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 552m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: PULLED BACK TO CASING SHOE. CIRCULATED UNTIL EVEN MUDWEIGHT AROUND AND FLUSHED KILL/CHOKE LINES. PERFORMED LEAK-OFF TEST TO 1,62 SG EMW." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: REPAIRED UPPER RACKING ARM: WELDED ON ANTI-TURN PADS FOR SWING MOTOR." "On 1992-11-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 633m. The activity was categorized as 'drilling -- drill' and lasted for 6.5 hours. Operational details: DRILLED/SURVEYED 17 1/2' FROM 552 TO 633M: STEERED FROM 562 TO 619M AND FROM 625 TO 633M." "On 1992-11-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 762m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONT. DRILLING/SURVEYING 17 1/2' HOLE TO 762M. STEERED FROM 633 TO 650M, 663M TO 684M, 692M TO 711M AND 721M TO 745M." "On 1992-11-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 780m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: DRILLED/SURVEYED 17 1/2' HOLE FROM 762 TO 780M. STEERED FROM 762 TO 772M" "On 1992-11-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 780m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: ATTEMPTED TO DUMP SHAKERBOX, NO-GO. UNPLUGGED DUMP LINE AND CLEANED OUT SHAKERBOX." "On 1992-11-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 780m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: REAMED FROM 720 TO 750M TO REDUCE DOG LEG." "On 1992-11-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 780m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: CHANGED SHAKER SCREENS AND CLEANED OUT SHAKER BOX." "On 1992-11-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 780m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: CONT. REAMING DOG LEG FROM 750 TO 780M." "On 1992-11-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1037m. The activity was categorized as 'drilling -- drill' and lasted for 13.0 hours. Operational details: DRILLED/SURVEYED 17 1/2' HOLE FROM 780 TO 1037M: STEERED 780-795M, 809-824M, 839-854M, 868-885M, 897-916M, 928-946M, 958-976M, 987-1006M AND 1016-1035M." "On 1992-11-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1044m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: CONT. ROTATION DRILLING AND SURVEYING TO 1044M." "On 1992-11-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1044m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: PULLED BACK TO 986M. REAMED DOG LEG TO 1044M." "On 1992-11-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1105m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: CONT. DRILLING/SURVEYING TO 1105M: STEERED FROM 1051-1068M AND 1077- 1094M." "On 1992-11-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1105m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: PULLED BACK TO 1044M. REAMED DOG LEG TO 1105M." "On 1992-11-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1117m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: CONT. DRILLING/SURVEYING TO 1117M: STEERED 1109-1117" "On 1992-11-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1395m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED/SURVEYED 17 1/2' HOLE FROM 1117M TO 1395M: STEERED FROM 1117 TO 1123M, 1132-1147M, 1162-1175M, 1191-1203M AND 1221-1233M." "On 1992-11-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1450m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONT. DRILLING/SURVEYING 17 1/2' HOLE TO 1450M: STEERED FROM 1415 TO 1425M AND 1447-1452M." "On 1992-11-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1490m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: CONT. DRILLING/SURVEYING 17 1/2' HOLE TO SECTION TD AT 1490M: STEERED FROM 1450 TO 1452M AND 1485 TO 1490M." "On 1992-11-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1490m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED" "On 1992-11-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1490m. The activity was categorized as 'drilling -- ream' and lasted for 8.0 hours. Operational details: BACK-REAMED FROM 1490M TO 533M." "On 1992-11-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 533m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE CLEAN" "On 1992-11-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 533m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: PULLED OUT OF HOLE. BROKE BIT, RACKED BACK BOTTOMHOLE ASSEMBLY. CHANGED SAVER SUB ON WAY OUT." "On 1992-11-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MADE UP PRE-LOADED CEMENT HEAD." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CONTINUED MAKING UP CEMENT HEAD. RACKED BACK HEAD IN DERRICK." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: MADE UP WIPER PLUGS, CASING HANGER AND SEAL ASSEMBLY TO SINGLE TRIP TOOL. RACKED ASSEMBLY IN DERRICK." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: MADE UP JET SUB. RAN IN HOLE AND WASHED WELLHEAD." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 221m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: MADE UP SPRING LOADED TOOL. RAN IN HOLE AND RETRIEVED 18 3/4' NOMINAL BORE PROTECTOR WITH 3 TONS OVERPULL. LAID DOWN BORE PROTECTOR AND TOOL. FLUSHED KILL AND CHOKE LINES. WASHED WELLHEAD ON WAY OUT." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 110m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: WASHED WELLHEAD, BOP AND RISER. LAID DOWN JET SUB." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: REMOVED STUCK DRIFT FROM PLUG LAUNCHER IN CASING HANGER JOINT." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: INSTALLED CASING STABBING BOARD. RIGGED UP TO RUN CASING." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: MADE UP TAM PACKER AND 5' PUP TO TDS." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 517m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: RAN SHOE JOINT, 1 CASING JOINT AND FLOAT JOINT AFTER HAVING CHECKED FLOATS. THREAD LOCKED SHOE JOINT AND FLOAT JOINT TO INTERMEDIATE JOINT. RAN 13 3/8' CASING TO 517M. FILLED CASING WITH 1,20 SG WHEN RUNNING IN HOLE." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 517m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOM UP AND CLEAN HOLE." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 517m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CHANGED TO 500 TON ELEVATOR AND SPIDER." "On 1992-11-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 739m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: CONTINUED RUNNING 13 3/8' CASING TO 739M." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1275m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONTINUED RUNNING 13 3/8' CASING TO 1275M." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1376m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RAN 13 3/8' CASING TO 1376 M." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: MAKE UP 13 3/8' CASING HANGER. RAN 13 3/8' CASING ON 5' HWDP. LANDED SAME. TOOK MEASUREMENTS." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS UP. PUMPED 25 M3 1,2 SG BENTONITE MUD. PRESSURE TESTED SURFACE LINE TO 345 BAR." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: PUMPED 12 M3 1,4 SG SPACER. MIXED AND PUMPED 71,8 M3 1,56 SG LEAD SLURRY,FOLLOWED BY 20,1 M3 1,9 SG TAIL SLURRY. DROPPED DART AND DISPLACED CEMENT WITH 1,5 M3 1,4 SG SPACER." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: DISPLACED CEMENT WITH 102,6 M3 1,2 SG MUD USING RIG PUMP. GOT CEMENT CONTAMINATED MUD IN RETURN OVER SHAKER. DID NOT BUMP PLUG." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1482m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: FLUSHED K/C LINE AND RISER. DUMPED CEMENT CONTAMINATED MUD. ATTEMPTED TO SET SEAL ASSY, NEGATIVE. RELEASED SEAL ASSY AND POOH WITH SAME." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 106m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: M/U MILL AND FLUSH TOOL. RIH AND WASHED SEAL AREA.GOT CMT CONTAMINATED MUD IN RETURN. POOH, L/D MILL AND FLUSH TOOL." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: M/U AND RIH W/SEAL ASSY. SET AND PRESSURE TEST SAME TO 140 BAR. RETORQUED SEAL ASSY AND PRESSURE TESTED TO 220 BAR. POOH AND L/D R/T." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: M/U JET SUB. RIH TO BELOW WELLHEAD. WASHED WELLHEAD/BOP AND RISER." "On 1992-11-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CHANGED BAILS." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: R/D CASING STABBING BOARD. BROKE PLUG LAUNCHER FROM SINGLE TRIP TOOL." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: MADE UP WEAR BUSHING TO SPRING LOADED TOOL. RIH AND SET 13 3/8' WEARBUSHING." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.0 hours. Operational details: PRESSURE TESTED BOP 20/220 BAR ON YELLOW POD, FUNCTION TEST BOP ON BLUE POD. FUNCTION TESTED ACOUSTIC SYSTEM." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: PULLED OUT OF HOLE WITH WEAR BUSHING RUNNING TOOL,JET SUB AND LAID DOWN SAME." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: PRESSURE TESTED LOWER/UPPER KELLY COCK, KELLY HOSE ON TOPDRIVE TO 20/220 BAR,OK." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: LAID DOWN 13 3/8' TAM PACKER AND CEMENT HEAD." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: LAID DOWN 17 1/2' BOTTOM HOLE ASSEMBLY." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: RIGGED UP ATLAS WIRE LINE." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- survey' and lasted for 6.0 hours. Operational details: RAN GYRO ON ATLAS WIRELINE.GYRO STOPPED AT 1407 M.CHECK LOGGED OUT OF HOLE.LAID DOWN GYRO." "On 1992-11-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1407m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RAN CBL. CBL LOG STOPPED AT 1407 M. LOGGED CBL." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONTINUED LOGGING CBL TO WELLHEAD. RIGGED DOWN ATLAS WIRELINE." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: MADE UP 12 1/4' BOTTOM HOLE ASSEMLY. CLOSED SHEAR RAM USING ACOUSTIC,PRESSURE TESTED 13 3/8' CASING TO 220 BAR,OK." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: REPAIRED SCR FOR MUD PUMP." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED TO MAKE UP 12 1/4' BOTTOM HOLE ASSEMLY. FUNCTION TESTED MUD MOTOR AND MWD." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1441m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: RIH WITH 12 1/4' BIT,TAGGED CEMENT AT 1441 M." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1441m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: PERFORMED BOP DRILL." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1490m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: DRILLED CEMENT,FLOAT AND SHOE AND CLEANED RAT HOLE." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1495m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 1490 M TO 1495 M." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1495m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED/CONDITIONED MUD.GOT 1,28 SG IN RETURNS,CIRCULATED UNTIL 1,25 SG IN/OUT." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1482m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: PERFORMED LOT WITH 1,25 SG MUD,EQUIVALENT TO 1,73 SG." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1551m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 1495 M TO 1551 M. STARTED TO DRILL WITH NEW 1,2 SG MUD." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: HAD BLACK OUT DUE TO GENERATOR OVERLOAD. CIRCULATED WITH NBS WHILE RESTARTED GENERATOR." "On 1992-11-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1637m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 1551 M TO 1637 M. ORIENTATED FROM 1585 M TO 1595 M." "On 1992-11-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1748m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 1637 M TO 1748 M. ORIENTATED FROM 1677 M TO 1691 M." "On 1992-11-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1981m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 1748 M TO 1981 M. ORIENTATED FROM 1926 M TO 1938 M (HS)." "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2018m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 1981 M TO 2018 M. ORIENTATED FROM 1988 M TO 2001 M (15R)." "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1985m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: BACKREAMED FROM 2018 M TO 1985 M. (POOH DUE TO LOW ROP)" "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- ream' and lasted for 7.5 hours. Operational details: BACKREAMED FROM 1985 M TO 13 3/8' SHOE AT 1482 M, CONTINUED BACKREAMING INSIDE CASING TO 800 W/HOLE ANGLE 20 DEG." "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED HOLE CLEAN. CIRCULATED RISER THROUGH KILL/CHOKE LINE." "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH,BROKE BIT." "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1983m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: MADE UP NEW BIT,REPLACED LOWER SLEEVE STABILIZER TO 12'. FUNCTION TESTED MOTOR/MWD,RIH TO 1983 M." "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2018m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: REAMED FROM 1983 M TO 2018 M AS PRECAUTION." "On 1992-12-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2041m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 2018 M TO 2041 M." "On 1992-12-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2166m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 2041 M TO 2166 M. ORIENTATED FROM 2132 M TO 2142 M (HS)." "On 1992-12-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2300m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 2166 M TO 2300 M. FLOWCHECKED DRILLING BREAK AT 2194 M,NEGATIVE." "On 1992-12-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2300m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED AND ROTATED DRILLSTRING DUE TO INADEQUATE HOLE CLEANING." "On 1992-12-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2470m. The activity was categorized as 'drilling -- drill' and lasted for 9.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 2300 M TO 2470 M. INCREASED MUDWEIGHT FROM 1,3 SG TO 1,4 SG,WHILE DRILLING FROM 2300 M TO 2383 M." "On 1992-12-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2465m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: REPAIRED TOP DRIVE DUE TO OVERLOAD ON ELECTRO MOTOR." "On 1992-12-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 2470 M TO 2531 M." "On 1992-12-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2531m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: CIRCULATED DUE TO OVERLOAD ON ELECTROMOTOR ON TOP DRIVE." "On 1992-12-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: PUMPED OUT OF HOLE DUE TO PROBLEMS WITH ELECTRO MOTOR ON TOP DRIVE." "On 1992-12-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1483m. The activity was categorized as 'interruption -- maintain' and lasted for 7.0 hours. Operational details: PUMPED OUT OF HOLE FROM 2100 M TO 1435 M. PACKED OFF AND CHARGED FORMATION AT 2094 M, 1830 M AND 1535 M. MAX GAS 2,2 %. RIH TO 1483 M." "On 1992-12-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1483m. The activity was categorized as 'interruption -- maintain' and lasted for 7.0 hours. Operational details: REPLACED OIL PUMP ON TOP DRIVE, DUE TO STUCK UPPER BEARING. CIRCULATED/ROTATED PIPE WHILE REPAIRED TOP DRIVE. PUMPED TWO 10 M3 HI-VIS PILLS GIVING LARGE AMOUNTS OF CUTTINGS IN RETURNS." "On 1992-12-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2215m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: TESTED MWD, PICKED UP 66 JOINTS 5' DRILL PIPE WHILE RIH FROM 1570 M TO 2215 M." "On 1992-12-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2531m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONTINUED RIH WITH STAND FROM 2215 M TO 2531 M." "On 1992-12-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2632m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 2531 M TO 2632 M." "On 1992-12-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2933m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 2632 M TO 2933 M. ORIENTATED FROM 2674 M TO 2684 M. (170L)" "On 1992-12-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3015m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 2933 M TO 3015 M. ORIENTATED FROM 2965 M TO 2972 M. (95R)" "On 1992-12-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3015 M TO 3017 M." "On 1992-12-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2460m. The activity was categorized as 'drilling -- ream' and lasted for 5.0 hours. Operational details: BACKREAMED FROM 3017 M TO 2460 M. PACKED OFF,AND CHARGED FORMATION." "On 1992-12-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2460m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: CIRCULATED HI-VIS PILL AROUND. NO INCREASING OF AMOUNT OFF CUTTINGS OVER SHAKER." "On 1992-12-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2120m. The activity was categorized as 'drilling -- ream' and lasted for 8.5 hours. Operational details: BACK REAMED FROM 2460 M TO 1960 M. HOLE PACKED OFF AT 2222 M,CHARGED FORMATION. ESTABLISHED CIRCULATION,PUMPED 10 M3 1,6 SG HI VIS PILL. HAD LARGE INCREASE IN CUTTINGS OVER SHAKER." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1926m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: BACK REAMED FROM 1960 M TO 1926 M." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1926m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: CHANGED WASH PIPE ON TOP DRIVE." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1926m. The activity was categorized as 'drilling -- ream' and lasted for 4.0 hours. Operational details: BACK REAMED FROM 1926 M TO 1482 M." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- ream' and lasted for 4.0 hours. Operational details: BACKREAMED FROM 13 3/8' SHOE AT 1482 M TO 800 M." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED HI VIS PILL AROUND.BOOSTED RISER." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: POOH. LAID DOWN BIT AND MUD MOTOR." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: CHANGED OUT MUD MOTOR,MAKE UP BIT.REPLACED JARS.TESTED MUD MOTOR AND MWD. RIH TO 1400 M." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: FUNCTION TESTED BOP AND ACOUSTIC SYSTEM, OK." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2876m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED RIH FROM 1400 M TO 2876 M." "On 1992-12-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3017m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: REAMED FROM 2876 M TO 3017 M, DUE TO TIGHT HOLE." "On 1992-12-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3026m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3017 M TO 3026 M." "On 1992-12-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3026m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: CHANGED PISTON ON MUDPUMP NO.1,SYLINDER NO.2. RECHARGED PULSATION DAMPENER WITH NITROGEN ON MUDPUMP NO.3. CIRCULATED/ROTATED WHILE REPAIRING MUDPUMPS." "On 1992-12-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3078m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3026 M TO 3078 M." "On 1992-12-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3257m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 3078 M TO 3257 M. ORIENTED FROM 3143 M TO 3150 M (180),FROM 3192 M TO 3198 M (120 L) REAMED EACH CONNECTION TWICE WITH 180 RPM ON STRING TO IMPROVE HOLE CLEANING." "On 1992-12-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3301m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 3257 M TO 3301 M. ORIENTED FROM 3284 M TO 3288 M. REAMED EACH CONNECTION TWICE WITH 180 RPM ON STRING TO IMPROVE HOLE CLEANING." "On 1992-12-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3353m. The activity was categorized as 'drilling -- drill' and lasted for 12.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 3301 M TO 3353 M. ORIENTED FROM 3284 M TO 3288 M(120L) AND FROM 3311 M TO 3321 M (120 L) REAMED EACH CONNECTION TWICE WITH 180 RPM ON STRING TO IMPROVE HOLE CLEANING." "On 1992-12-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3353m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED AND ROTATED STRING 180 RPM.PUMPED 8 M3 1,6 SG HI VIS PILL." "On 1992-12-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3100m. The activity was categorized as 'drilling -- ream' and lasted for 4.0 hours. Operational details: BACK REAMED FROM 3353 M TO 3100 M." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2830m. The activity was categorized as 'drilling -- ream' and lasted for 4.5 hours. Operational details: BACK REAMED FROM 3100 M TO 2830 M. PUMPED 8 M3 1,6 SG HI VIS PILL AT 3035 M" "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2866m. The activity was categorized as 'drilling -- ream' and lasted for 1.5 hours. Operational details: PACKED OFF AT 2830 M,WORKED/ROTATED PIPE DOWN TO 2866 M. NO RETURN." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2904m. The activity was categorized as 'drilling -- ream' and lasted for 2.0 hours. Operational details: WORKED/ROTATED PIPE FROM 2866 M TO 2904 M. ESTABLISHED CIRCULATION." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2904m. The activity was categorized as 'drilling -- ream' and lasted for 3.0 hours. Operational details: CIRCULATED, BOOSTED RISER BY PUMPING DOWN KILL/CHOKE LINE USING CEMENT PUMP." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2904m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: HOLE PACKED OFF AT 2904 M. WORKED PIPE AND ESTABLISHED CIRCULATION." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2904m. The activity was categorized as 'drilling -- ream' and lasted for 4.5 hours. Operational details: ESTABLISHED FULL CIRCULATION (2700 LTR/MIN). PUMPED 10 M3 1,18 SG KCL PILL, FOLLOWED BY 8 M3 1,6 SG HI VIS PILL. CIRCULATED SAME OUT." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2924m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: CIRCULATED AND WORKED/ROTATED PIPE UP/DOWN FROM 2900 M TO 2924 M. BEAKREAMED FROM 2924 M TO 2900 M. LOST RETURN." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2904m. The activity was categorized as 'drilling -- ream' and lasted for 2.0 hours. Operational details: WORKED PIPE TO ESTABLISH FULL CIRCULATION." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2925m. The activity was categorized as 'drilling -- ream' and lasted for 5.0 hours. Operational details: CIRCULATED AND WORKED/ROTATED PIPE UP/DOWN FROM 2900 M TO 2925 M. ADDED KCL AND EZ MUD DP DIRECTLY INTO ACTIVE MUD SYSTEM." "On 1992-12-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2880m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: BACK REAMED FROM 2900 M TO 2880 M." "On 1992-12-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2732m. The activity was categorized as 'drilling -- ream' and lasted for 4.0 hours. Operational details: BACK REAMED FROM 2880 M TO 2732 M." "On 1992-12-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2741m. The activity was categorized as 'drilling -- ream' and lasted for 2.0 hours. Operational details: HOLE PACKED OFF AT 2732 M,WORKED PIPE DOWN TO 2741 M. HAD FULL RETURN WITH MAX 1400 LTR/MIN,NO ROTATION." "On 1992-12-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2741m. The activity was categorized as 'interruption -- fish' and lasted for 12.0 hours. Operational details: ATTEMPTED TO WORK PIPE FREE AT 2741 M,MAX OVERPULL/DOWNWEIGHT 175/40 TON. MAX TORQUE 33000 FT-LBS. CIRCULATED WITH MAX 2900 LTR/MIN. PUMPED 9 M3 1,11 SG KCL PILL,FOLLOWED BY 1,6 SG HI VIS PILL,PUMPED SAME OUT.PUMPED 9 M3 1,03 SG LO VIS PILL,FOLLOWED BY 1,6 SG HI VIS PILL." "On 1992-12-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2741m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: CONTINUED TO WORK PIPE FREE AT 2741 M,MAX PULL/DOWNWEIGHT 175/40 TON,MAX TORQUE 33000 FT-LBS. CIRCULATED WITH MAX 2900 LTR/MIN." "On 1992-12-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2741m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: CONTINUED TO WORK PIPE FREE AT 2741 M,MAX OVERPULL/DOWNWEIGHT 170/40 TON,MAX TORQUE 33000 FT-LBS. CIRCULATED WITH MAX 2900 LTR/MIN." "On 1992-12-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2741m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: PUMPED 18 M3 1,45 SG EZ SPOT PILL, DISPLACED SAME WITH 18 M3 1,4 SG MUD. SPOTTED 10,3 M3 AROUND BHA, LEFT 7,7 M3 INSIDE PIPE." "On 1992-12-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2741m. The activity was categorized as 'interruption -- fish' and lasted for 3.0 hours. Operational details: CONTINUED TO WORK PIPE FREE AT 2741 M,MAX PULL/DOWNWEIGHT 175/40 TON. MAX TORQUE 33000 FT-LBS. PUMPED 210 LTR EZ SPOT PILL EVERY 1/2 HRS." "On 1992-12-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2741m. The activity was categorized as 'interruption -- fish' and lasted for 5.5 hours. Operational details: CONT. ATTEMPTING TO WORK PIPE FREE, NEGATIVE. MOVED EZ-SPOT EVERY HALF HOUR BY PUMPING 210 LITERS." "On 1992-12-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2652m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: CHANGED TO 500 TON LINKS AND RIGGED UP ATLAS WIRELINE. RAN IN WITH JRC CUTTER AND CCL AT 14:30 HRS. WITH 50 TONS OVERPULL ON STRING, DETONATED CHARGE AT 2658,2M. PIPE NOT FREE. POOH WITH WIRELINE. FOUND JRC TOOL, X-OVER TO SAME AND 1 SINKER BAR TO BE LEFT IN HOLE." "On 1992-12-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2658m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: CIRCULATED 2000 STROKES: SURFACE PUMPING PRESSURE 100 BAR LESS THAN BEFORE CUTTING AND NO COMMUNICATION WITH MWD. ATTEMPTED TO WORK STRING FREE FROM THE BHA BY APPLYING UP TO 34000 FTLBS TORQUE AND 180 TONS OVERPULL, NO SUCCESS." "On 1992-12-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2510m. The activity was categorized as 'interruption -- fish' and lasted for 4.0 hours. Operational details: RIGGED UP WIRELINE. RAN FREE-POINT INDICATOR. CHECKED AND CALIBRATED TOOL AT 1400M, OK. RAN IN TO 2512M, TOOL FAILURE. POOH." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: FOUND SHORT ON MONOCONDUCTOR EXTENSION CABLE. CUT OFF DAMAGED CABLE AND RETERMINATED." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2584m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: RAN IN WITH FREE-POINT INDICATOR AND CCL. CHECKED AND CALIBRATED TOOL AT 1400M, OK. FOUND 5' DP TO BE FREE. CHECKED INSIDE HWDP AT 2530 AND 2584M, POSSIBLY FREE. POOH." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: PREPARED TO RUN IN WITH JRC CUTTER AND CCL." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2516m. The activity was categorized as 'interruption -- fish' and lasted for 4.5 hours. Operational details: RAN IN WITH JRC CUTTER AND CCL. DETONATED CUTTER AT 2516M, KEPT 50 T OVERPULL ON STRING. POOH WITH WIRELINE." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2516m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: PULLED PIPE FREE WITH 100 T OVERPULL. CIRCULATED BU." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2516m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: POOH. MAX. BREAK-OUT TORQUE 80000 FTLBS. LD STUFFING BOX AND CIRCULATION SUB." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: CHANGED BAILS AND ELEVATOR." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: SLIPPED AND CUT 32M DRILL LINE." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: CLEARED RIG FLOOR. INSPECTED AND LUBRICATED TDS." "On 1992-12-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 80m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: MU BHA FOR SIDE TRACK." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1266m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.0 hours. Operational details: CONT. MU BHA FOR SIDE TRACKING. DRIFTED AND SERVICE BROKE CONNECTIONS ON HWDP. RAN IN TO 1266M. LOST RETURNS." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: WORKED PIPE AND BROKE CIRCULATION, OK. WASHED/REAMED FROM 1266M TO 1390M." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2220m. The activity was categorized as 'drilling -- ream' and lasted for 6.0 hours. Operational details: CONTINUED REAMING FROM 1390 TO 2220M. HOLE PACKED OFF. LOST RETURNS AND UNABLE TO ROTATE STRING." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2188m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: WORKED PIPE BACK TO 2188M. ROTATED STRING AND RE-ESTABLISHED FULL CIRCULATION." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2188m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED AND CLEANED HOLE." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2188m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: DISPLACED HOLE TO 1,50 SG NEW KCL MUD." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2188m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: CHANGED SAVER SUB AND LOWER VALVE IN TDS." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2188m. The activity was categorized as 'drilling -- ream' and lasted for 1.0 hours. Operational details: BACK-REAMED FROM 2188 TO 1971M." "On 1992-12-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1971m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: POOH" "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1971m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONT. POOH. RACKED BACK BHA." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: MU CEMENT HEAD. RACKED SAME BACK IN DERRICK." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1640m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: RAN IN WITH OPEN ENDED 5' DP TO 1640M. LOST RETURNS." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1640m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: WORKED PIPE. CIRCULATED 800 STROKES, MAX. 60 SPM, FULL RETURNS." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1902m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CONT. RUNNING IN TO 1902M, LOST RETURNS." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2020m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: WORKED PIPE AND CIRCULATED 40 SPM, FULL RETURNS. CONT. RUNNING IN TO 2020M." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2220m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CONT. RI TO 2220M." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2220m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CIRCULATED. INCREASED RATE SLOWLY UP TO 2800 LPM." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2220m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: PUMPED 4 M3 HI-VIS 1,5 SG KCL MUD. DISPLACED SAME WITH 19,5 M3 MUD." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2220m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: PULLED BACK TO 2180M. HOOKED UP CEMENT HOSE, PRESSURE TESTED CEMENT LINES TO 100 BAR/5 MINS. PUMPED 3,0 M3 FRESH WATER, 15,2 M3 1,95 SG CEMENT, 430 L FRESH WATER, DROPPED WIPER PLUG AND DISPLACED CEMENT WITH 17,3 M3 1,5 SG MUD. ROTATED STRING DURING DISPLACEMENT." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2180m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: PULLED BACK TO 1850M." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1850m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: CIRCULATED HOLE CLEAN." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1850m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: PUMPED 3,0 M3 FRESH WATER, 22,8 M3 1,5 SG CEMENT, 350 L FRESH WATER. DISPLACED WITH 14 M3 MUD." "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1410m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: PULLED BACK TO 1410M" "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1410m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CIRC. BU" "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1410m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: POOH" "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: BROKE OUT 12 1/4' BIT. REARRANGED BHA IN DERRICK" "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: LD CEMENT HEAD" "On 1992-12-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: MU 12 1/4' CLEAN-OUT ASSEMBLY AND RAN IN HOLE" "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: CONT RIH TO 1400M" "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1493m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: FILLED PIPE. WASHED/REAMED FROM 1400M TO 1493M. PIPE STUCK AT 1493M WITHOUT ANY WARNING SIGNS. KEPT FULL CIRCULATION." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1496m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: WORKED PIPE FREE. WORKED PIPE ACROSS TIGHT AREAS AT 1492M TO 1494M. TENDENCIES OF GETTING STUCK SEVERAL TIMES. CONTINUED WORKING PIPE. NO CEMENT IN RETURNS. WORKED PIPE TO 1496M. FULL CIRCULATION AT ALL TIMES." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1510m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: CONT. WASHING/REAMING TO 1510M." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1510m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CIRCULATED WHILE MIXING HI-VIS 1,75 SG PILL." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1510m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: SWEPT PILL AROUND AND WASHED/REAMED TO 1540M. TOOK WEIGHT." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1540m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: BACK-REAMED TO 1483M." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1483m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CIRCULATED BU" "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1483m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: BACK-REAMED TO 1000M." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CIRCULATED HOLE CLEAN" "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.5 hours. Operational details: POOH. LD STABILISER/1 EACH 8' DC/NB STABILISER/BIT." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: MU PRE-LOADED CEMENT HEAD, RACKED SAME IN DERRICK." "On 1992-12-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: RIH WITH 5' OEDP. BROKE CIRCULATION AT 1150M." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1470m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CONT. RIH WITH 5' OEDP TO 1470M." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1543m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: WASHED/ROTATED FROM 1470 TO 1543M. WORKED THROUGH SPOTS AT 1529 AND 1535M. TOOK WEIGHT AT 1543M. PULLED BACK TO 1527M." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1527m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: RU CEMENT EQUIPMENT. PRESSURE TESTED SURFACE LINES TO 100 BAR/10 MINS. RAN IN TO 1541M." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1541m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: PUMPED 3,0 M3 FRESHWATER. MIXED AND PUMPED 10,4 M3 1,95 SG CEMENT, PUMPED 420 L FRESH WATER. DROPPED WIPER PLUG. DISPLACED WITH 12,2 M3 MUD." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1541m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: DISCONNECTED CEMENT HOSE AND RACKED BACK CEMENT HEAD. PULLED BACK TO 1400M." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CIRCULATED BU." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: PUMPED SLUG AND POOH TO 1300M." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CONT. POOH." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: RIH AND WASHED BOP AND WELLHEAD. INSTALLED TEST TOOL AND 1 STAND 5' DP" "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: LD CEMENT HEAD" "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 6.0 hours. Operational details: PRESSURE TESTED BOP TO 20/220 BAR, 5/10 MINS. PRESSURE TESTED STAND PIPE, INSIDE BOP AND SPARE KELLY COCK TO 35/345 BAR, 5/10 MINS. BOP WAS FUNCTIONED ON BLUE POD. FUNCTION TESTED BOP ON ACOUSTIC SYSTEM." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1377m. The activity was categorized as 'interruption -- sidetrack' and lasted for 8.5 hours. Operational details: MU BHA. TESTED MWD AND MUD MOTOR. CHANGED OUT JARS. PU 6 5/8' HWDP. RI TO 1377M." "On 1992-12-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: DISPLACED WELL TO SEA WATER." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CONT. DISPLACING TO SEA WEATER" "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1474m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: WASHED/REAMED FROM 1400M TO 1474M. INDICATION OF CEMENT FROM 1460 M. 1,5 - 2 TON WEIGHT." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: FLUSHED THROUGH SURFACE LINES, CHOKEMANIFOLD. CLANED OUT SHAKERPITS, TRIPTANK, POORBOY DEGASSER AND MUD SURFACE SYSTEM. PLUGGED OFF ALL DRAINS." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1470m. The activity was categorized as 'drilling -- drill' and lasted for 12.5 hours. Operational details: CONTINUED PREPARATIONS FOR PETROFREE MUD: CLEANED SHAKER PITS AND MUD PITS. PLUGGED OFF DRAINS. STARTED OFFLOADING MUD FROM BOAT." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1470m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: PUMPED 9 M3 SPACER AND DISPLACED WELL TO 1,35 SG PETROFREE MUD." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1470m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED TO CONDITION MUD WHILE FILLING SHAKERPITS AND SURFACE EQUIPMENT WITH MUD." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1486m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: WASHED/REAMED FROM 1474M TO 1478M. WITH PUMPS OFF, SET DOWN 5 TONS ON CEMENT. DRILLED CEMENT TO 1486M." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1486m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: WHILE PUMPING 2500 LPM, CHECKED TOOLFACE FOR 20 MINUTES, NEG. PULLED BACK INTO CASING. STOPPED PUMPS 2 MINUTES WHILE LINING UP FOR RETURNS OVER SHAKERS." "On 1992-12-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1470m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: HOLE PACKED OFF. UNABLE TO CIRCULATE/ROTATE. WORKED PIPE FREE WITH 40 TONS OVERPULL." "On 1992-12-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1470m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: PULLED BACK TO 1435M. LOOSING MUD WHEN CIRCULATING AT 1620LPM." "On 1992-12-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: PULLED BACK TO 1400M. CIRCULATED UP TO 2600 LPM, FULL RETURNS." "On 1992-12-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1482m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: WASHED/REAMED FROM 1400 TO 1482M." "On 1992-12-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1493m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.0 hours. Operational details: WASHED/REAMED TO 1486M. DRILLED CEMENT FROM 1486M TO 1493M." "On 1992-12-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1493m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP." "On 1992-12-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1493m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: PRESSURE TESTED SURFACE LINES TO 100 BAR/10 MINS. PERFORMED F.I.T. TO 1,65 SG EQUIVALENT MUD WEIGHT." "On 1992-12-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1536m. The activity was categorized as 'interruption -- sidetrack' and lasted for 12.0 hours. Operational details: SIDETRACKED AND DRILLED 12 1/4' HOLE. DRILLED/SURVEYED FROM 1493M TO 1536M: STEERED FROM 1493 TO 1507M, 1509-1511M, 1513-1523M AND 1531-1536M. (100-120 DEG.RIGHT TF) INCREASED MW FROM 1,35 TO 1,40 SG.WHILE DRILLING." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1588m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONT. DRILLING/SURVEYING 12 1/4' HOLE TO 1588M: STEERED FROM 1536M TO 1551M AND 1562M TO 1580M. (80-85 DEG. RIGHT TOOLFACE)" "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1630m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.0 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 1588M TO 1630M: STEERED FROM 1589 TO 1608M, 100 DEGREES RIGHT." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1630m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP DUE TO EXCESSIVE AMOUNT OF CUTTINGS OVER SHAKERS." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1630m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: BACKREAMED FROM 1630M TO 1485M." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1485m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1630m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: RIH TO 1630M." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1653m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 1630M TO 1653M: STEERED FROM 1643M TO 1653 M, TOOLFACE 110 DEG. LEFT. OBSERVED 70 BAR INCREASE IN PUMP PRESSURE." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1653m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: PUMPED 3 M3 ESTER PILL. SWEPT PILL AROUND, NO EFFECT." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1653m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: BACKREAMED FROM 1653M TO 1000M." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE CLEAN. HAD HIGH AMOUNT OF CUTTINGS OVER THE SHAKERS FROM CASING. PUMPED SLUG." "On 1992-12-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: POOH" "On 1992-12-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.0 hours. Operational details: CONTINUED POOH. INSPECTED BHA FOR DAMAGE/BLOCKAGE. FOUND 2 NOZZLES PLUGGED WITH FLAKE OF REINFORCED RUBBER FROM MUD MOTOR. LAID DOWN MUD MOTOR AND BIT. RACKED BACK MWD IN DERRICK." "On 1992-12-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: MADE UP NEW MUD MOTOR AND BIT. TESTED MUD MOTOR. RIH WITH BHA." "On 1992-12-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: CONTINUED MAKING UP BOTTOMHOLE ASSEMBLY. ORIENTED TOOL FACE. RAN IN TO 250M. ATTEMPTED TESTING THE MWD TOOL, NEGATIVE." "On 1992-12-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: POOH. LAID DOWN MWD TOOL. PICKED UP A NEW MWD TOOL AND TESTED SAME. RAN BACK IN TO 250M." "On 1992-12-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1485m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: CONTINUED RIH TO 1485M. FILLED PIPE AT 700M." "On 1992-12-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1653m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: REAMED HOLE FROM 1485M TO 1653M." "On 1992-12-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1799m. The activity was categorized as 'interruption -- sidetrack' and lasted for 8.5 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 1653M TO 1799M: STEERED FROM 1653 TO 1658M (120 DEGR. LEFT), 1665-1679 (120 L), 1694-1709 (80 L), 1723-1738 (110 L), 1752-1767 (110 L) AND 1780-1795 (110 L)." "On 1992-12-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1926m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING/SURVEYING 12 1/4' HOLE FROM 1799M TO 1926M: STEERED FROM 1809M TO 1824M (DIRECTION 115 DEGREES LEFT)." "On 1992-12-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2241m. The activity was categorized as 'interruption -- sidetrack' and lasted for 18.0 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 1926M TO 2241M: STEERED FROM 1982M TO 1992M (DIRECTION 90 DEGREES RIGHT)." "On 1992-12-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2357m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING 12 1/4' HOLE FROM 2241M TO 2357M: STEERED FROM 2242M TO 2248M (DIRECTION 120 DEGREES RIGHT)." "On 1992-12-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2502m. The activity was categorized as 'interruption -- sidetrack' and lasted for 9.0 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 2357M TO 2502M: STEERED FROM 2385M TO 2392M (DIRECTION 130 DEGREES RIGHT)" "On 1992-12-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2502m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP" "On 1992-12-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2502m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.5 hours. Operational details: BACK-REAMED FROM 2502M TO 13 3/8' SHOE AS PRECAUTION." "On 1992-12-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1485m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP" "On 1992-12-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1485m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: INVESTIGATED ALARM ON TDS. FOUND AIR BLOWER HOSE TO HAVE JUMPED OFF. RE-INSTALLED SAME." "On 1992-12-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2502m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: RAN BACK IN TO 2502M. FILLED PIPE AND CIRCULATED A RISER VOLUME AT 1950M." "On 1992-12-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2559m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 2502M TO 2559M: STEERED FROM 2502M TO 2510M (DIRECTION 75 DEGREES RIGHT)" "On 1992-12-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2840m. The activity was categorized as 'interruption -- sidetrack' and lasted for 18.0 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 2559M TO 2840M: STEERED FROM 2559 TO 2568M (DIRECTION 90 DEGREES RIGHT) AND FROM 2763 TO 2775M (HIGH SIDE)." "On 1992-12-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2938m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING/SURVEYING 12 1/4' HOLE TO 2938M." "On 1992-12-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3018m. The activity was categorized as 'interruption -- sidetrack' and lasted for 10.0 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 2938M TO 3018M." "On 1992-12-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3018m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP" "On 1992-12-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3018m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: BACKREAMED FROM 3018M TO 2952M. HOLE PACKED OFF. LOST RETURNS. UNABLE TO ROTATE." "On 1992-12-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2968m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.5 hours. Operational details: RAN IN FROM 2952M TO 2968M. ESTABLISHED ROTATION AND CIRCULATION. ONLY PARTIAL RETURNS WHEN PUMPING MORE THAN 1200 LPM." "On 1992-12-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3017m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.5 hours. Operational details: RAN IN TO 3017M. PUMPED AND SET 7,1 M3 LIQUID CASING LCM-PILL FROM 3017M TO 2927M WHILE PULLING BACK TO 2957M, FULL RETURNS. AT 2957M, HOLE PACKED OFF. UNABLE TO ROTATE. RAN BACK IN TO 2963M." "On 1992-12-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2963m. The activity was categorized as 'interruption -- lost circulation' and lasted for 1.0 hours. Operational details: AT 2963M, REESTABLISHED ROTATION AND CIRCULATION. KEEPING 40 RPM ON THE DRILL STRING, INCREASED CIRCULATION RATE IN STEPS TO 1300 LPM, FULL RETURNS." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.0 hours. Operational details: CONTINUED INCREASING CIRCULATION RATE TO 1900LPM, FULL RETURNS." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2963m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.5 hours. Operational details: INCREASED CIRCULATION RATE TO 2600 LPM, FULL RETURNS. KEPT 40 RPM ON DRILL STRING." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2963m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: BACKREAMED OUT OF HOLE FROM 2963M TO 2941M." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2941m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CONTINUED BACKREAMING FROM 2941M TO 2936M. HOLE PACKED OFF AND STRING STALLED OUT. ATTEMPTED WORKING PIPE DOWN WITH 40 TONS, NO-GO. ATTEMPTED TO JAR DOWN, NO-GO. ATTEMPTED WORKING PIPE DOWN WITH TORQUE, NO-GO. PULLED 60 TONS OVERPULL ON PIPE. WORKED PIPE DOWN TO 2941M. REESTABLISHED ROTATION AND CIRCULATION." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.0 hours. Operational details: CIRCULATED AND ROTATED PIPE AT 2941M. INCREASING AMOUNT OF CUTTINGS OVER SHAKERS. WORKED PIPE DOWN TO 2961M." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: PUMPED 10 M3 LO-VIS PILL FOLLOWED BY 10 M3 HI-VIS PILL, CIRCULATED PILLS AROUND." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED CIRCULATING. RAISED MUDWEIGHT TO 1,45 SG." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: PUMPED 20 M3 HI-VIS 1,6 SG PILL. CIRCULATED SAME AROUND." "On 1992-12-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: CIRCULATED TO RECORD CUTTINGS RETURNS." "On 1992-12-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: CONTINUED CIRCULATING HOLE." "On 1992-12-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2961m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: CIRCULATED AND RAISED MUDWEIGHT TO 1,50 SG." "On 1992-12-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2967m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.5 hours. Operational details: CIRCULATED WHILE WORKING PIPE FROM 2967M TO 2941M. RECORDED CUTTINGS RETURNS." "On 1992-12-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2967m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: CIRCULATED HOLE AND RAISED MUDWEIGHT TO 1,55 SG." "On 1992-12-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2967m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.5 hours. Operational details: CIRCULATED HOLE WHILE RECORDING CUTTINGS RETURNS OVER SHAKER. WORKED PIPE BETWEEN 2967M AND 2941M WHILE CIRCULATING." "On 1992-12-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2941m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: BACKREAMED FROM 2941M TO 2913M AT 2700LPM, 150 RPM. TDS STALLED OUT AT 2917M. WORKED PIPE DUE TO TIGHT HOLE." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2913m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CONTINUED BACKREAMING TO 2910M. WORKED PIPE DUE TO TIGHT HOLE." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2910m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS UP WHILE WORKING PIPE BETWEEN 2939M AND 2910M." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2910m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.5 hours. Operational details: CONTINUED BACKREAMING FROM 2910M TO 2850M. WORKED PIPE DUE TO TIGHT HOLE. TDS STALLED OUT AT 2899M. CIRCULATED 15 MINUTES ON CONNECTION." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2850m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: BACKREAMED FROM 2850M TO 2837M. WORKED PIPE DUE TO TIGHT HOLE." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2837m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP DUE TO HIGH AMOUNT OF CUTTINGS OVER SHAKERS." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2837m. The activity was categorized as 'interruption -- sidetrack' and lasted for 13.5 hours. Operational details: BACKREAMED FROM 2837M TO 2730M. WORKED PIPE DUE TO TIGHT HOLE." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2730m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CIRCULATED BOTTOMS UP." "On 1992-12-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2730m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: BACKREAMED FROM 2730M TO 2715M. WORKED PIPE DUE TO TIGHT HOLE." "On 1992-12-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2715m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED BACKREAMING FROM 2715M TO 2608M. CIRCULATED 20 TO 15 MINS. ON EACH CONNECTION. WORKED PIPE IN TIGHT SECTIONS. TIGHT HOLE TO 2701M. TIGHT SPOTS TO 2608M." "On 1992-12-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2608m. The activity was categorized as 'interruption -- sidetrack' and lasted for 10.5 hours. Operational details: BACKREAMED FROM 2608M TO 2320M. MAX TOURQUE 14000 NM." "On 1992-12-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2320m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CIRCULATED HOLE AND STARTED INCREASING MUD WEIGHT TO 1.60 S.G." "On 1992-12-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2320m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.5 hours. Operational details: BACKREAMED FROM 2320M TO 1661M. MAX TORQUE 14000 NM." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1661m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: BACKREAMED FROM 1661M TO 1590M. MAX TORQUE 10000 NM. LARGE AMOUNTS OF CUTTINGS STARTED COMMING OVER THE SHAKERS AND A SLIGHT PRESSURE INCREASE WAS OBSERVED." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1590m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE UNTIL CUTTINGS LEVEL CAME DOWN AND NO PRESSURE INCREASE WAS OBSERVED WHILE PULLING THE STAND OUT." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1590m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.5 hours. Operational details: BACKREAMED FROM 1590M TO 1475M. MAX TORQUE 10000 NM." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1475m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: BACKREAMED FROM 1475M TO 1440M." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1615m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: RIH TO 1615M, NO TIGHT SPOTS. POOH TO 1445M." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1445m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: BACKREAMED FROM 1445M TO 950M." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.5 hours. Operational details: SLUGED PIPE. POOH. LAID DOWN 12 1/4' BOTTOM HOLE ASSEMBLY." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CLEANED ESTER MUD ON RIG FLOOR." "On 1992-12-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 840m. The activity was categorized as 'interruption -- sidetrack' and lasted for 7.0 hours. Operational details: MADE UP NEW BHA AND RAN IN HOLE TO 840M." "On 1992-12-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2740m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.0 hours. Operational details: CONTINUED RUNNING IN HOLE FROM 840M TO 2740M. WASHED PAST SPOT AT 2650M." "On 1992-12-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2903m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: WASHED DOWN FROM 2740M TO 2780M. CONTINUED RIH FROM 2780M TO 2903M. WASHED PAST SPOT AT 2825M." "On 1992-12-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2965m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CONTINUED RIH FROM 2903M TO 2965M." "On 1992-12-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3018m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.0 hours. Operational details: REAMED/WASHED FROM 2965M TO 3018M. TIGHT SPOT AT 2965M." "On 1992-12-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3043m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: DRILLED/SURVEYED 12 1/4' HOLE FROM 3018M TO 3043M." "On 1992-12-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3050m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3043M TO 3050M WITH LIMITED PENETRATION- RATE. VARIED DRILLING PARAMETRES WITHOUT ANY APPARENT GAIN." "On 1992-12-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3050m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: BACKREAMED FROM 3050M TO 2778M. MAX TORQUE 15000 NM. RPM 140. PUMP PRESSURE 200 BAR AT 128 SPM." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2778m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CONTINUED BACKREAMING FROM 2778M TO 2691M. MAX TORQUE 15000 NM. RPM 140. PUMP PRESSURE 200 BAR AT 128 SPM." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2691m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.0 hours. Operational details: CONTINUED BACKREAMING FROM 2691M TO 2130M. MAX TORQUE 15000 NM. RPM 140. PUMP PRESSURE 180 BAR AT 128 SPM." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2130m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.0 hours. Operational details: CONTINUED BACKREAMING FROM 2130M TO 1069M. WORKING TIGHT SPOTS AT 1972M AND 1685M." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1069m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.0 hours. Operational details: POOH, CHANGED BIT AND MWD PRS-SUB." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: RECHECK ALIGMENT BETWEEN MUDMOTOR AND MWD TOOL, THIS DUE TO A DIFFERENCE OF 30 DEG. BETWEEN BHA NO.11 AND BHA NO.12. THE SAME TOOL WAS USED IN BOTH BHA'S." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1480m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: RIH TO 1480M BREAKING CIRCULATION EVERY 500M." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1480m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: SLIPPED AND CUT DRILLINE. SERVICED TOP DRIVE." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1480m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: TOOK PRESSURE READINGS FOR HYDRAULIC CALCULATIONS." "On 1992-12-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2983m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: CONTINUED RIH FROM 1480M TO 2983M BREAKING CIRCULATION EVERY 500M." "On 1993-01-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3050m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: WASHED/REAMED FROM 2983M TO 3050M. TIGHT SPOT AT 2925M." "On 1993-01-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3050m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: ATTEMPTED TO GET SURVEY, NEG. (TO MUCH NOISE FROM SYSTEM)" "On 1993-01-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3052m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3050M TO 3052M WITH LIMITED PENETRATION- RATE. VARIED ALL DRILLING PARAMETERS WITH NO APPARENT GAIN." "On 1993-01-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3052m. The activity was categorized as 'interruption -- sidetrack' and lasted for 7.5 hours. Operational details: POOH. WORKED TIGHT SPOT AT 2993M. FLOWCHECKED AT SHOE-NEG." "On 1993-01-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: LAID DOWN MUD MOTOR." "On 1993-01-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- bop activities' and lasted for 8.0 hours. Operational details: MADE UP BOP TEST-TOOL. RIH AND TEST BOP TO 20 BAR / 200 BAR. POOH WITH TEST TOOL." "On 1993-01-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 37m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: MADE UP NEW BIT AND MUD MOTOR. RIH TO 37M. TESTED MUD MOTOR AND MWD." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2207m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED RIH FROM 37M TO 2207M. BROKE CIRCULATION EVERY 500M." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2956m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CONTINUED RIH FROM 2207M TO 2956M." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3050m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: REAMED DOWN FROM 2956M TO 3050M." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3082m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3050M TO 3082M. FLOW CHECKED DRILLING BRAKE AT 3063M - NEG." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3099m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: DRILLED/STEARED 12 1/4' HOLE FROM 3082M TO 3099M. HAD PROBLEMS RECIEVING TOOL PHASE READINGS, AND STALLING OF BIT. PROBLEM TIME 70 MIN." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3099m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: REAMED ONE STAND FOR GAMMA RAY LOG. USED 20 MIN TO OBTAIN SURVEY AT 3084M. TO IDENTIFY BOTTOM SAND." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3137m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.0 hours. Operational details: DRILLED/STEARED 12 1/4' HOLE FROM 3099M TO 3137M. LOST 20 MIN TRYING TO ESTABLISH TOOL PHASE." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3137m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: UNABLE TO OBTAIN TOOL PHASE FOR STEARING. MUD PUMP NO 1 DOWN. TO MUCH NOISE IN SYSTEM TO OBTAIN READABLE SIGNAL FROM MWD." "On 1993-01-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3137m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: PULLED UP TO 2990M TO CIRCULATE BOTTOMS UP. WORKED PAST SPOT AT 3050M. STARTED CIRCULATING HOLE CLEAN. 0.5KG INCREASING TO 11KG CUTTINGS PER 15 SECONDS." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2990m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: CONTINUED CIRCULATING HOLE CLEAN AT 2990M. MAX AMOUNT OF CUTTINGS OVER SHAKER 19KG PER 15 SECONDS. STOPPED WHEN LEVEL CAME DOWN TO 4,9 KG. CIRCULATED WITH 144 SPM ON DP, 50 SPM ON RISER AND 160 RPM. ESTIMATED AMOUNTS OF CUTTINGS CIRCULATED OUT 10M3." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2990m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: POOH FROM 2990M TO 2738M. TIGHT SPOT AT 2982M." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2738m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CONTINUED PULLING UP FROM 2738M TO 2500M." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3137m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: RAN BACK IN HOLE TO TD AT 3137M." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3141m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3137M TO 3141M." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3141m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: ATTEMPTED TO GET SURVEY NEG. MWD TOOL FAILURE." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3141m. The activity was categorized as 'interruption -- sidetrack' and lasted for 7.5 hours. Operational details: POOH TO CHANGE MWD TOOL." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: CLEANED ESTER MUD ON RIG FLOOR AND UNDER ROTARY." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- sidetrack' and lasted for 5.5 hours. Operational details: PICKED UP NEW MWD AND PRS-SUB AND RIH TO 1343M." "On 1993-01-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: PICKED UP HANG-OFF STAND AND PREPARED TO HANG OFF DUE TO WEATHER CONDITIONS." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1447m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: HUNG OFF DRILL STRING IN WELLHEAD AND RETRIEVED HANG OFF STRING." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1447m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: DISPLACED RISER TO SEA WATER." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.5 hours. Operational details: W.O.W. SEE REMARKS FOR DETAILS." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.0 hours. Operational details: W.O.W, SEE REMARKS FOR DETAILS." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: POSITIONED RIG BACK OVER TEMPLATE." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: DISPLACED RISER BACK TO 1.6 S.G. MUD." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1447m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: RETRIEVED DRILLSTRING FROM WELLHEAD." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1447m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: POOH WITH HANG OFF ASSEMBLY, REDRESSED SAME." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1343m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: REPAIRED UPPER RACKING ARM." "On 1993-01-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3141m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: RIH FROM 1343M TO 3141M. WORKED TIGHT SPOT AT 2980M. REAMED LAST STAND TO TD." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3141m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: UNABLE TO OBTAIN READABLE SIGNALS FROM MWD. 45 MIN LOST TIME." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3157m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3141M TO 3157M." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3157m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: TROUBLESHOOTING SYSTEM TO GET READABLE DATA FROM MWD. UNABLE TO DETECT SOURCE OF PROBLEM. OBTAINED SURVEY BY USING MUDPUMP NO.3 AT 115 STKS. SUCTION MODULE ON MUD PUMP NO.1 DEVELOPED A LEAK, HAD TO BE CHANGED OUT." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3166m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3157M TO 3166M." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3166m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: TOOK SURVEY AT 3143M. HAD PROBLEMS WITH MWD SIGNAL." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3166m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: PUMP NO.3 LOST SUCTION DUE TO LEAK IN SUPERCHARGE FILTERBOX." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3168m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: STEARED 12 1/4' HOLE FROM 3166M TO 3168M. WITH GOOD SIGNALS FROM MWD. USING MUD PUMP NO.2 AT 125 STKS." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3174m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: DRILLED/ORIENTATED 12 1/4' HOLE FROM 3168M TO 3174M. GOOD MWD READINGS. USED MUD PUMP NO.2 AT 2020LPM." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3174m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: TOOK SCR. LINED UP MUD PUMPS NO.2 AND 3." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3188m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3174M TO 3188M. DRILLING PARAMETERS: 160 RPM, 2330LPM, 265BAR." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3188m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: ATTEMPTED TO TAKE SURVEY, NEGATIVE. LOST 40 MINUTES." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3195m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3188M TO 3195M." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3198m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: TOOK SURVEY AT 3195M. ORIENTATED FROM 3195M TO 3198M. USED MUD PUMP NO.2 AT 2020LPM. CHANGED TO MUD PUMP NO.3 AT 3196M DUE TO WASHOUT IN VALVE ON PUMP NO.2. HAD CONTINOUSLY PROBLEMS WITH LOCKING ON TO MWD SIGNAL AND WITH MUD MOTOR STALLING OUT. LOST 1,5 HRS. FINALLY MANAGED TO ORIENTATE USING BOTH MUD PUMPS NO.2 AND 3." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3202m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3198M TO 3202M. DRILLING PARAMETERS: 2390LPM, 270BAR. NO GAMMA RAY OR DIRECTIONAL DATA OBTAINED." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3204m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.0 hours. Operational details: ORIENTATED 12 1/4' HOLE FROM 3202M TO 3204M. HAD PROBLEMS WITH DIRECTIONAL DATA AND WITH MUDMOTOR STALLING OUT. LOST 1,5 HRS ON ACTUAL SURVEY PROBLEMS." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3204m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: POOH TO 2898M. TIGHT SPOTS AT 3046M AND 3010M. STARTED CIRCULATING BUTTOMS UP WITH 2556LPM, 270BAR, 165RPM." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2898m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.0 hours. Operational details: CIRCULATED HOLE CLEAN. MAX AMOUNT OF CUTTINGS OVER SHAKERS WAS 8,7 KG/15 SEC. CIRCULATION RATE 2500 LTRS ON DP AND 750 LTRS ON RISER. 160 RPM ON STRING. RACKED TWO STANDS BACK WHILE REAMING." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2842m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: ANADRILL REPLACED TRANSDUCER ON TOP OF STANDPIPE. PUMPED THROUGH CEMENT HOSE ON PUMP-IN SUB WHILE RECIPROCATING STRING. PUMP SPEED 1600 LPM." "On 1993-01-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2842m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: STARTED PULLING UP TO 2500M FROM 2842M TO PERFORM TESTS ON ANADRILL MWD EQUIPMENT." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2621m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: FINISHED PULLING UP TO 2500M FROM 2621M TO PERFORM TESTS ON ANADRILL MWD EQUIPMENT." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2500m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: TESTED MWD EQUIPMENT WITH VARYING PUMPING SPEEDS. EQUIPMENT FUNCTIONING PROPERLY, ABLE TO GET BOTH SURVEYS AND TOOLPHASE." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3204m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: RIH FROM 2500M TO 3204M. WORKED TIGHT AREA FROM 2974M TO 2985M." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3204m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: ATTEMPTED TO ORIENT 12 1/4' HOLE, BUT HAVING PROBLEMS KEEPING TOOLPHASE. MWD LOGGING UNIT IS RECIEVING TO MUCH NOISE. TOOLPHASE IS OBTAINED WHEN TOOL IS STATIONARY. WHEN MOVING DP, TOOLPHASE FLUCTUATES AND WHEN BIT IS ON BOTTOM TOOLPHASE IS LOST. INCREASE IN PRESSURE ON BOTTOM IS 5 BAR." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3214m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: ORIENTATED 12 1/4' HOLE FROM 3204M TO 3214M. HAVING SYNCHRONIZING PROBLEMS WITH MWD." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3215m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: ORIENTATED 12 1/4' HOLE FROM 3214M TO 3215M. HAVING SYNCHRONIZING PROBLEMS WITH MWD AND BIT STALLING OUT." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3215m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: POOH TO 2495M. WORKED TIGHT SPOTS AT 3030M, 2990M AND 2965M." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2495m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE CLEAN. MAX AMOUNT OVER SHAKER DURING CIRCULATION 6,8 KG/15 SEC. CIRCULATION RATE 2675 LPM ON DRILLSTRING, 750 LPM ON RISER. 180 RPM." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2495m. The activity was categorized as 'interruption -- sidetrack' and lasted for 7.0 hours. Operational details: POOH." "On 1993-01-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: LAID DOWN ANADRILL MWD EQUIPMENT." "On 1993-01-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2963m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: PICKED UP NEW BIT AND TELECO MWD-TOOL. RIH TO 2963M. NO TIME LOST RIGGING UP TELECO EQUIPMENT." "On 1993-01-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3215m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: FINISHED RIH TO 3215M. REAMED LAST STAND." "On 1993-01-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3303m. The activity was categorized as 'interruption -- sidetrack' and lasted for 16.5 hours. Operational details: DRILLED AND ORIENTATED 12 1/4' HOLE FROM 3215M TO 3303M. REAMED TWICE AFTER EACH STAND DRILLED. ORIENTATED WITH 2150LPM / 240-250BAR. DRILLED WITH 2270LPM / 270BAR / 160 RPM, PROBLEMS WITH STALLING FROM 3235M TO 3237M. DRILLED HARD STRINGERS AND HAD PROBLEMS BUILDING ANGLE FROM 3290M TO 3296M." "On 1993-01-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3303m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: REAMED AND CIRCULATED WITH 2300 LPM/170 RPM WITH NO APPERENT INCREASE IN TORQUE READINGS. MAX AMOUNT CUTTINGS OVER SHAKERS: 11,5 KG/15 SEC." "On 1993-01-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3311m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: ORIENTATED 12 1/4' HOLE FROM 3303M TO 3311M. 2200 LPM / 240-250BAR. DRILLED THROUGH HARD STRINGERS AT 3308M AND 3310M." "On 1993-01-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3315m. The activity was categorized as 'interruption -- sidetrack' and lasted for 1.0 hours. Operational details: HAD TO DRILL THROUGH A HARD SECTION FROM 3311M TO 3315M. USING 2200LTRS / 165 RPM / MAX 15TONN." "On 1993-01-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3321m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: ORIENTATED 12 1/4' HOLE FROM 3315M TO 3321M. HAD STALLING PROBLEMS FROM 3316M TO 3319M." "On 1993-01-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3321m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CIRCULATED TO CLEAN HOLE, PUMPING 2307 LPM WITH 260 BAR." "On 1993-01-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3331m. The activity was categorized as 'interruption -- sidetrack' and lasted for 2.5 hours. Operational details: DRILLED AND ORIENTATED FROM 3321 TO 3331 M. HAD STALLING PROBLEMS IN STEERING MODE." "On 1993-01-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3331m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: WORKED PIPE AND CIRCULATED HOLE CLEAN, PUMPING 2326 LPM WITH 260BAR AND 172 RPM. MAX CUTTINGS OVER SHAKERS 15,4 KG/15 SEC." "On 1993-01-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3389m. The activity was categorized as 'interruption -- sidetrack' and lasted for 12.0 hours. Operational details: DRILLED AND ORIENTATED FROM 3331 TO 3389 M. HAD STALLING PROBLEMS IN STEERING MODE." "On 1993-01-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3436m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING AND ORIENTATING FROM 3389 TO 3436 M. HAD STALLING PROBLEMS WHEN STEERING." "On 1993-01-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3475m. The activity was categorized as 'interruption -- sidetrack' and lasted for 4.5 hours. Operational details: CONT DRILLING 12 1/4' HOLE FROM 3436 TO 3475 M. ATTEMPTED TO ORIENTATE AT 3460 M." "On 1993-01-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3475m. The activity was categorized as 'interruption -- sidetrack' and lasted for 3.0 hours. Operational details: WORKED PIPE AND CIRCULATED HOLE CLEAN, PUMPING 2390 LPM WITH 172 RPM AND 273 BAR. MAX CUTTINGS OVER SHAKERS IN END OF DRILLING 18 KG/15 SEC MAX CUTTINGS DURING CIRC 9,7 KG/15 SEC." "On 1993-01-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3562m. The activity was categorized as 'interruption -- sidetrack' and lasted for 10.0 hours. Operational details: DRILLED FROM 3475 TO 3562 M. ATTEMPTED TO ORIENTATE AT 3461 M. ORIENTATED FROM 3509 TO 3513,5 M. HAD DRILLING BREAKE AT 3489 M - FLOWHECKED." "On 1993-01-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3562m. The activity was categorized as 'interruption -- sidetrack' and lasted for 0.5 hours. Operational details: CIRCULATED HOLE CLEAN, PUMPING 2270 LPM WITH 172 RPM AND 260 BAR." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3562m. The activity was categorized as 'interruption -- sidetrack' and lasted for 6.0 hours. Operational details: CONTINUED HOLE CLEANING, PUMPING 2270 LPM WITH 172 RPM AND 260 BAR. MAX CUTTINGS OVER SHAKERS 17,2 KG/15 SEC. STARTED TREATED MUD AT 0500 HRS." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3562m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: CONTINUED CIRCULATING FOR HOLE CLEANING AND TREATED MUD. PUMPED 2206 LPM WITH 164 RPM AND 244 BAR. MAX CUTTINGS OVER SHAKERS 2,2 KG/15 SEC." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED 12 1/4' HOLE FROM 3562 TO 3580 M. DRILLING BREAK AT 3570 M." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.5 hours. Operational details: CIRCULATED BOTTOMS UP FOR FORMATION SAMPLE. PUMPED 2200 LPM, 20 AND 160 RPM." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- trip' and lasted for 4.0 hours. Operational details: POOH TO 2100 M TO RUN 9 5/8' CSG. REAMED THROUGH TIGHT SPOT AT 3025 M." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2100m. The activity was categorized as 'drilling -- wait' and lasted for 0.5 hours. Operational details: SECURED EXLOG HOSE TO KELLY HOSE." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1300m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONT POOH TO 6 STDS ABOVE 13 3/8' CSG SHOE. FLOWCHECKED 20 MIN WHILE M/U HANG-OFF TOOL." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: RIH WITH HANG-OFF TOOL. RELEASED TOOL. BIT DEPTH 1390 M." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: POOH WITH LANDING STRING." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: DISPLACED RISER TO SEAWATER." "On 1993-01-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: WAITING ON WEATHER." "On 1993-01-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONT WAITING ON WEATHER, FOR DETAILS SEE GERERAL REMARKS." "On 1993-01-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: WAITED ON WEATHER FOR WEATHER DETAILS, SEE GENERAL REMARKS." "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONT WAITING ON WEATHER." "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: CONTINUED WAITING ON WEATHER." "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: P/U 9 5/8' CSG HANGER AND PLUGS, M/U TO RUNNING TOOL. RACKED HANGER ASSY BACK IN DERRICK." "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1390m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 3.0 hours. Operational details: RIH WITH HANG-OFF RETRIEVING TOOL TO 101 M. DISPLACED RISER TO 1,60 SG MUD. ENGAGED DRILL STRING AND POOH WITH RETRIEVING TOOL." "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1490m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: RIH TO 1490 M." "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1490m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED AND CONDITIONED MUD" "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONT RIH FROM 1490 TO 3580 M. BROKE CIRC EVERY 500 M. REAMED TIGHT SPOT AT 3009 M." "On 1993-01-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: CIRCULATED AND TREATED MUD." "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3570m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.5 hours. Operational details: CONT CIRCULATION AND TREATED MUD, REDUSED MW FROM 1,62 TO 1,60 SG. PUMPED 2200 LPM WITH 264 BAR AND 135 RPM." "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3480m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: FLOWCHECKED 10 MIN, POOH TO RUN 9 5/8' CASING, AT 3480 M." "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 9.0 hours. Operational details: CONT POOH WITH 12 1/4' BIT FROM 3480 M. BACKREAMED FROM 3030 TO 2990 M FLOWCHECKED AT 2350 AND 1475 M. L/D BIT AND BHA, DUMPED MEMORY ON MWD TOOL." "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: RIH WITH JET SUB AND WASHED BOP/WH, M/U SPRING LOADED TOOL AND CONT RIH AND RETRIEVED WEAR BUSHING. PERFORMED 'VETCO' MEASUREMENTS." "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: REPAIRED UPPER RACKING ARM" "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH, L/D WB. WASHED WH SEAL AREA AND BOP AND CONT POOH." "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: R/U TO RUN 9 5/8' CASING, INST TAM TOOL. HELD PRE-JOB MEETING WITH CREW" "On 1993-01-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 76m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RAN SHOE JNT, 1 CSG JNT AND FLOAT JNT, CHECKED FLOAT. THREAD LOCKED SHOE JNT AND FLOAT JNT TO INTERMEDITATE JNT. RAN 9 5/8' CSG TO 76 M. FILLED EVERY JNT WITH 1,60 SG MUD." "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 810m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONTINUED RUNNING 9 5/8' CASING FROM 76 TO 810 M. RECORDED UP AND DOWN WT." "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 980m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: CONT RUNNING 9 5/8'CASING FROM 810 TO 980 M." "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 980m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: REPAIRED GANTRY CRANE" "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1460m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: CONT RUNNING CASING FROM 980 TO 1460 M." "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1460m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: INSTALLED TAM PKR, CIRC HOLE SLOWLY AT 80 LPM INCRASING TO 275 LPM. RECORDED LOSS. CHECKED SURFACE PITS FOR LEAKS. MONITORED WELL ON TRIP TANK, WELL STATIC, NO LOSS TO FORMATION DURING CIRCULATION." "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1460m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PROBLEMS TO RESET TAM PACKER" "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1460m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: INSTALLED TAM-PKR. INCREASED PUMP RATE IN STEPS OF 80 LPM TO 598 LPM. HAD FULL RETURNS, CIRC BOTTOMS UP" "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1460m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: INSTALLED 500 MT ELEVAT0R AND SPIDER" "On 1993-01-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2210m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONT RUNNING CASING FROM 1460 TO 2210 M" "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2747m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONT RUNNING CASING FROM 2210 TO 2747 M" "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3228m. The activity was categorized as 'drilling -- casing' and lasted for 6.5 hours. Operational details: CONT RUNNING 9 5/8' CASING FROM 2747 TO 3228 M HELD OPERATION MEETING WITH CREW." "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3228m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: ENGAGED TAM-PACKER. BROKE CIRCULATION GENTLY, CIRCULATED WHILE WOW. PREPARED 10 3/4' CSG EQUIP." "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3390m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: CONT RUNNING CASING FROM 3228 TO 3390 M" "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3390m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: REPLACED 9 5/8' CSG EQUIP WITH 10 3/4' CSG EQUIP. M/U X-OVER HELD OPERATION MEETING WITH CREW" "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH WITH 10 3/4' CASING FROM 3390 TO 3442 M" "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3442m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: R/D 10 3/4' CASING EQUIP AND R/U 6 5/8' DP EQUIP" "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RAN 10 3/4' CASING HANGER AND LANDING STRING. LANDED HANGER AT 2140 HRS WITH 9 5/8' SHOE AT 3569,3 M" "On 1993-01-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: CIRCULATED WELL, REDUCED MW FROM 1,60 TO 1,55 SG. TREATED MUD FOR MUD PROPERTIES" "On 1993-01-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONT CIRCULATION TO REDUCE MW FROM 1,60 TO 1,55 SG. TREATED MUD. PUMPED 810-1437 LPM WITH 34-45 BAR" "On 1993-01-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 7.5 hours. Operational details: CONT CIRCULATION TO REDUCE MW FROM 1,60 TO 1,55 SG. TREATED MUD. PUMPED 1440 LPM WITH +- 40 BAR" "On 1993-01-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: PUMPED 30 M3 1,55 SG OMC-2 TREATED PETROFREE MUD FOLLOWED BY 44 M3 1,55 SG BENTONITE MUD" "On 1993-01-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: PUMPED 11,5 M3 1,70 SG SPACER. DROPPED BALL FOR BOTTOM PLUG. MIXED AND PUMPED 32 M3 1,94 SG CEMENT SLURRY. DROPPED DART AND DISPLACED CEMENT WITH 1,3 M3 MIX WATER AND 2,0 M3 1,55 SG PETROFREE MUD." "On 1993-01-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: DISPLACED CEMENT WITH 1,55 SG PETROFREE MUD PUMPING WITH RIG PUMPS. PRESS BUILD UP TO 190 BAR AFTER 89,9 M3 PUMPED. CALCULATED VOLUME 126,2 M3 TO BUMP PLUG." "On 1993-01-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: CHECKED OUT SURFACE EQUIPMENT. BLEED OFF PRESS TO 20 BAR, RECIEVED 1200 LTR BACK. CHECKED OUT AND FOUND ALL CEMENT TO BE LEFT IN CASING. PRESS UP CSG TO 300 BAR ATTEMPTING TO OPEN UP CASING - NEG. BLEED OFF PRESSURE." "On 1993-01-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: R/D SURFACE EQUIP, BACKED OUT FMC SINGLE TRIP RUNNING TOOL FROM HANGER POOH AND L/D SEAL ASSY" "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: L/D CMT HEAD AND X-OVERS. CHANGED ELEVATOR LINKS, R/D STABBING BOARD. R/U HEAD ON LOWER RACKING ARM." "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: M/U AND RIH WITH JET SUB, WASHED WH AREA, M/U WEAR BUSHING AND CONT RIH, SET WB AND POOH" "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: P/U AND M/U NEW 8 1/2' BHA." "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CONT M/U 8 1/2' BHA. NOT ABLE TO INSTALL FLOAT, REPLACED BIT SUB AND FLOAT." "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 115m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: CONT M/U BHA AND RIH TO 115 M." "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.0 hours. Operational details: POOH DUE TO BAD WEATHER" "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 8.0 hours. Operational details: DISPLACED RISER TO SW. PREPARED TO UNLATCH LMRP, CLOSED SHEAR-RAM. UNLATCHED LMRP AT 1640 HRS. DEBALLASTED RIG TO SURVIVAL DRAFT. PULLED RIG 25 M OFF LOCATION." "On 1993-01-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.5 hours. Operational details: WAITED ON WEATHER" "On 1993-01-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONT WAITING ON WEATHER" "On 1993-01-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 13.0 hours. Operational details: CONTINUED WAITING ON WEATHER" "On 1993-01-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: DEBALLASTED RIG TO 21 M AND PULLED RIG ON LOCATION" "On 1993-01-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: CLEARED OUT GUIDELINES AROUND BOP STACK WITH ROV. INSTALLED NEW GUIDELINE NO 2 WITH ROV" "On 1993-01-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: INSTALLED DIVERTER HANDLING TOOL." "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: RELEASED DIVERTER AND PREPERED TO LAND LMRP." "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: BALLASTED RIG TO DRILLING DRAFT" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: RI AND LANDED LMRP, PULLTESTED WITH 25 MT. INSTALLED DIVERTER ELEMENT AND L/D HANDLING TOOLS" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: PRESS TESTED BOP KILL AND CHOKE STABS.345 BAR/10 MIN" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: DISPLACED RISER TO 1,55 SG PETROFREE MUD" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: RETRIEVED WEAR BUSHING" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: M/U CEMENT CLEANOUT TOOL AND RIH. WASHED WELLHEAD AND POOH" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: M/U SEAL ASSY, RIH AND INSTALLED IN WH. PRESS TESTED SEAL ASSY TO 345 BAR" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: PRESS TESTED BOP ON BLUE POD" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: ATTEMPTED TO OPERATE FAILSAFE - NEG. SEARCED FOR MALFUNCTION AND FOUND BOOSTER BOTTLES ON BOP NOT CHARGED. OPENED ACCUMULATOR ISOLATOR AND CONTINUED PRESS TESTING BOP." "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: PRESS TESTED BOP. FUNCTION TESTED ACOUSTIC SYSTEM." "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: PULLED OUT BOP TEST TOOL" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: PRESS TESTED SHEAR RAM 345 BAR." "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RUN AND INSTALLED WEAR BUSHING" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: SERVICE-BROKE TAM-PACKER, L/D ON DECK" "On 1993-01-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: M/U 8 1/2' BIT, BHA AND RIH TO DRILL CMT IN 9 5/8' CASING BROKE CIRC EVERY 500 M" "On 1993-01-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2502m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: CONT RIH FROM 170 TO 2502 M BROKE CIRC EVERY 500 M" "On 1993-01-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2510m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: DRILLED DART PLUG FROM 2502 M, CONTINUED DRILLING CMT FROM 2502,5 TO 2510 M" "On 1993-01-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2937m. The activity was categorized as 'drilling -- casing' and lasted for 18.0 hours. Operational details: CONTINUED DRILLING WITH 8 1/2' BIT IN 9 5/8' CASING FROM 2510 TO 2937 M" "On 1993-01-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3040m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING CEMENT FROM 2937 TO 3040 M" "On 1993-01-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3391m. The activity was categorized as 'drilling -- casing' and lasted for 18.0 hours. Operational details: CONTINUED DRILLING CEMENT WITH 8 1/2' BIT IN 9 5/8' CASING FROM 3040 TO 3391 M" "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONT DRILLING CMT IN 9 5/8' CASING FROM 3391 TO 3422 M" "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3280m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: CIRCULATED 15 MIN AND BACKREAMED 5 STDS, CONTINUED CIRC HOLE CLEAN DUE TO BAD WEATHER." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: M/U TIW AND HANG-OFF TOOL. RI AND HANG-OFF IN WH, POOH DISPLACED RISER TO SEAWATER AND CLOSED S/R PREPARED TO UNLATCH LMRP" "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: WAITED ON WEATHER. DE-BALLASTED RIG 2,1 M." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.5 hours. Operational details: RE-BALLASTED RIG TO DRILLING DRAFT. OPENED SHEAR RAM AND DISPLACED RISER BACK TO 1,55 SG MUD." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: RAN IN TO WELLHEAD AND RECONNECTED TO DRILL STRING. RACKED HANG-OFF STAND IN DERRICK. L/D INSIDE BOP." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3422m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RAN IN TO 3393M. WASHED TO 3422M." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3452m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: DRILLED CEMENT FROM 3422M TO 3452M." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3452m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP" "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3543m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RAN IN TO 3543M. TOOK WEIGHT." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: DRILLED WIPER PLUG, FLOAT AND SHOE. CLEANED RAT HOLE." "On 1993-01-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PULLED BACK INTO 9 5/8' CASING. CIRCULATED BOTTOMS UP." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3560m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CONTINUED CIRCULATING HOLE CLEAN. SLUGGED PIPE." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3560m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: POOH. RACKED BHA IN DERRICK. BROKE BIT." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 5.0 hours. Operational details: RIGGED UP WIRELINE. RIH WITH GYRO, UNABLE TO PASS 1230M. POOH." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2675m. The activity was categorized as 'drilling -- survey' and lasted for 4.5 hours. Operational details: MADE UP 8 1/2' BIT AND 9 5/8' CASING SCRAPER. RAN IN TO 2675M. BROKE CIRCULATION AT 1200 AND 2400M." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2675m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: TOOK WEIGHT UP TO 20 MT FROM 2503 M TO 2675 M. CIRC. BOTTOMS UP TO CLEAN HOLE." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3545m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: CONTINUED RUNNING IN TO 3545M." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3545m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: WORKED CASING SCRAPER FROM 3525M TO 3545M. CIRCULATED HOLE CLEAN AND CONDITIONED MUD." "On 1993-01-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2052m. The activity was categorized as 'drilling -- survey' and lasted for 3.0 hours. Operational details: POOH FROM 3545M." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1300m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: CONTINUED POOH TO 1300M." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1030m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: PUMPED OUT OF HOLE FROM 1300M TO 1030M." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1030m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED BOTTOMS UP." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- survey' and lasted for 2.0 hours. Operational details: CONTINUED POOH. BROKE BIT AND CASING SCRAPER. RACKED BHA." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: RIGGED UP FOR WIRELINE." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- survey' and lasted for 6.0 hours. Operational details: RAN GYRO TO 3500M. POOH AND L/D TOOL. R/D WIRELINE" "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U JET TOOL. WASHED WELLHEAD. L/D JET TOOL." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: M/U BAKER CEMENT RETAINER AND RIH TO 85M. PIPE DID NOT FILL. POOH AND L/D RETAINER." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 8.0 hours. Operational details: M/U ALPHA CEMENT RETAINER AND RIH TO 3535M." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RELEASED SLIPS AND SET RETAINER BY PULLING 20 TONS OVERPULL. SET DOWN 10 TONS TO VERIFY SETTING, OK." "On 1993-01-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: LINED UP TO PRESSURE TEST CEMENT RETAINER. FLUSHED LINES AND ATTEMPTED PRESSURE TESTING SURFACE LINES AGAINST FAIL SAFE VALVE TO 100 BAR, NEGATIVE. TESTED CEMENT UNIT, OK. LINED OVER FROM TEST LINE TO CEMENT LINE AND ATTEMPTED PRESSURE TESTING AGAINST FAIL SAFE, NEG." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3525m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: PRESSURE TESTED CEMENT RETAINER AGAINST UAP TO 70 BAR/10 MINS, OK. RELEASED RUNNING TOOL AND STINGED OUT OF RETAINER. BROKE CIRCULATION AT 25-30 BAR WITH CEMENT UNIT." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH WITH 5 STANDS. M/U PULLING TOOL. RIH AND RETRIEVED WEAR BUSHING. L/D SAME." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RAN IN TO RETRIEVE SEAL ASSEMBLY. LATCHED INTO SAME. CLOSED UAP AND PULLED SEAL ASSEMBLY FREE. NO OVERPULL. NO GAS OR PRESSURE BELOW SEAL ASSEMBLY. CIRCULATED THROUGH BOP. OPENED UAP AND PULLED OOH WITH SEAL ASSEMBLY. L/D SEAL ASSEMBLY AND PULLING TOOL." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3522m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RAN IN TO 3522M. HOOKED UP CEMENT HOSE AND LINED UP TO ESTABLISH CIRCULATION BEHIND CASING." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: M/U CIRC. SUB AND CEMENT HOSE. PRESSURE TESTED SURFACE LINES TO 250 BAR/5 MINS. BROKE CIRCULATION. STINGED INTO RETAINER AND SAT DOWN 10 TONS ON SAME. ATTEMPTED TO ESTABLISH CIRCULATION BEHIND CASING, NEGATIVE." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3372m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: DISCONNECTED CEMENT HOSE. PULLED BACK TO 3372M. PREPARED FOR RUNNING SEAL ASSEMBLY." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3372m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WAITED ON WEATHER." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 35m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: ATTEMPTED TO RUN IN WITH SEAL ASSEMBLY. HUNG UP AT 35M. POOH. FOUND SEALS DAMAGED. L/D SEAL ASSEMBLY AND RUNNING TOOL." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: RAN IN TO 3530M. HOOKED UP CEMENT HOSE AND PRESSURE TESTED SURFACE LINES TO 345 BAR/5 MINS. PUMPED 1,0 M3 MIXING WATER AS SPACER. MIXED AND PUMPED 4,0 M3 1,9 SG CEMENT. PUMPED 0,5 M3 SPACER. DISPLACED SAME WITH 24,0 M3 MUD AT 600 LPM. STINGED INTO RETAINER. SQUEEZED CEMENT INTO FORMATION BY PUMPING 6,0 M3 MUD AT 400 LPM/160 BAR." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 0.0 hours. Operational details: STINGED OUT OF RETAINER. PUMPED 0,5 M3 MUD. PULLED BACK TO 3452M." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3452m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CIRCULATED ANY EXCESS CEMENT BEYOND 3000M. PUMPED 8,0 M3 2,0 SG HI-VIS PILL. DISPLACED SAME WITH 29,0 M3 MUD." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3270m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PULLED BACK TO 3270M." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3270m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CIRCULATED OUT ANY EXCESS PILL." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2985m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: SLUGGED PIPE. POOH TO 2985M." "On 1993-01-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2985m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: DRIVE GEAR FOR JAW ON UPPER RACKING ARM WORN OUT. ATTEMPTED REPAIR, NEGATIVE." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2985m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: CONT. ATTEMPTS TO REPAIR JAW, NEGATIVE. RIGGED UP TO PULL STANDS MANUALLY." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2985m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: POOH TO 750M. PULLED STANDS IN DERRICK MANUALLY." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 750m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONT. POOH. L/D CEMENT STINGER" "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: ATTEMPTED TO RELEASE JAMMED SEAL ASSEMBLY FROM RUNNING TOOL, NEGATIVE." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH WITH CEMENT CLEAN-OUT TOOL. HUNG UP AT 34 M. WORKED TOOL THROUGH RESTRICTION. WASHED WELLHEAD AND POOH." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: CLEANED RIG FLOOR." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: M/U ELASTOMERIC SEAL ASSEMBLY AND RUNNING TOOL AND RIH. HUNG UP AT 34 M. WORKED THROUGH RESTRICTION. SET SEAL ASSEMBLY. FLUSHED LINES. PRESSURE TESTED SURFACE LINES TO 345 BAR/5 MINS. PRESSURE TESTED SEAL ASSEMBLY TO 345 BAR/10 MINS. RELEASED RUNNING TOOL AND POOH." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: SET WEAR BUSHING." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIGGED UP WIRELINE. PREPARED AND ARMED GUNS." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 34m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: ATTEMPTED TO RUN IN WITH GUNS, NEGATIVE. HUNG UP AT 34 M. POOH. INSTALLED CENTRALIZER." "On 1993-01-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3260m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RAN IN WITH PERFORATING GUNS. CORRELATED AND PERFORATED 9 5/8' CASING FROM 3260 TO 3255,4M. POOH." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3260m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONT. POOH WITH GUNS. ALL SHOTS FIRED. R/D WIRELINE." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3260m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: FLUSHED K/C-LINES. VERIFIED OPEN PERFORATIONS BY INJECTING MUD WITH CEMENT PUMP AGAINST SHEAR RAM." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1700m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: M/U ALPHA CEMENT RETAINER. HUNG UP AT 34 M. WORKED RETAINER THROUGH RESTRICTION. RAN IN TO 1700M. ROTATED 1-2 REVOLUTIONS TO THE LEFT EACH 10 STANDS TO PREVENT SLIPS FROM SETTING PREMATURELY. RUNNING SPEED 90 SEC/STD." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: CONT. RIH WITH ALPHA CEMENT RETAINER." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: SET PACKER AT 3225M. FLUSHED SURFACE LINES AND PRESSURE TESTED RETAINER DOWN ANNULUS TO 70 BAR/10 MINS." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RE-CHECKED PERFORATIONS BY INJECTING 0,5 M3 MUD." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: ATTEMPTED TO RELEASE RUNNING TOOL, NEGATIVE. INCREASED OVERPULL IN STEPS UP TO 40 TONS. ROTATED STRING WITH OVERPULL. WHILE ROTATING, REDUCED OVERPULL IN STEPS UNTIL NEUTRAL AND SLACKED DOWN UNTIL WEIGHT DOWN. WORKED PIPE UP/DOWN WHILE ROTATING, CAME FREE WITH 20 T OVERPULL. PRESSURE TESTED RETAINER TO 95 BAR/10 MINS." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- casing' and lasted for 0.0 hours. Operational details: STUNG INTO RETAINER AND CONFIRMED INJECTIVITY. PULLED OUT OF RETAINER WHILE PUMPING TO VERIFY PROPER FUNCTIONING, OK." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: INSTALLED CEMENT HOSE. FLUSHED/PRESSURE TESTED SURFACE LINES TO 345 BAR/5 MINS. PUMPED 3,0 M3 UNWEIGHED SPACER. MIXED AND PUMPED 7,5 M3 1,9 SG CEMENT SLURRY. PUMPED 1,0 M3 UNWEIGHED SPACER. DISPLACED SAME WITH 16,9 M3 1,55 BENTONITE MUD. STINGED INTO RETAINER. SQUEEZED 5,0 M3 CEMENT SLURRY BY PUMPING 9,0 M3 BENTONITE MUD." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3225m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: HESITATION SQUEEZED 1,0 M3 CEMENT SLURRY. STINGED OUT OF RETAINER. PUMPED 0,5 M3 MUD. PULLED BACK TO 3210M." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3210m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 3.0 hours. Operational details: DISPLACED HOLE TO 1,55 BENTONITE MUD." "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3210m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D CIRCULATING EQUIPMENT. R/U TO L/D PIPE" "On 1993-01-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3210m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: POOH. L/D DP." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3210m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: CONT. POOH. L/D 85 JOINTS." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: CONT. POOH WITH STINGER TO 200M." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 200m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: CONT. POOH. L/D CEMENT STINGER." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PRESSURE TESTED 9 5/8' CASING TO 345 BAR/15 MINS." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 205m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.5 hours. Operational details: M/U BAKER 2C-2P RETRIEVABLE ABANDONMENT PLUG. RAN IN HOLE AND SET PLUG AT 205M. PRESSURE TESTED PLUG TO 100 BAR FOR 15 MINS. PULLED BACK 3 M." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 202m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: DISPLACED HOLE TO INHIBITED SEA WATER. L/D BAKER RUNNING TOOL." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: SLIPPED DRILL LINE." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: R/U TO PULL BOP. L/D DIVERTER. INSTALLED HANDLING JOINT. DEBALLASTED RIG 10 FT. UNLATCHED BOP AND PULLED SAME ABOVE TEMPLATE." "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.5 hours. Operational details: MOVED RIG 25M OFF LOCATION" "On 1993-01-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: RE-BALLASTED RIG TO DRILLING DRAFT. DISCONNECTED RUCKER TENSIONERS. REMOVED POD LINE SADDLES AND K/C-LINES. PULLED BOP TO SURFACE. DE-BALLASTED RIG 10 FT DUE TO HIGH SEAS. LANDED BOP ON CARRIER." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: SECURED BOP ONTO CARRIER. L/D 2 EA 50 FT RISER JOINTS." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RE-BALLASTED RIG TO DRILLING DRAFT. R/D RISER HANDLING EQUIPMENT. R/U PIPE HANDLING EQUIPMENT." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: CLEANED RIG FLOOR." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: M/U RUNNING TOOL FOR TEMPORARY ABANDONMENT CAP." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: MADE UP TEMPORARY ABANDONMENT CAP TO RUNNING TOOL AND RAN IN TO 82M." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.5 hours. Operational details: MOVED RIG OVER WELL" "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: INSTALLED CAP ON WELLHEAD. PUMPED STACK-MAGIC CORROSION INHIBITOR. RELEASED RUNNING TOOL, PULLED BACK TO 80M." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 95m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: PULLED GUIDE WIRE 3 AND 4. RELEASED GUIDE WIRE 1, CLOSED HATCH WITH SAME. PULLED GUIDE WIRE 1." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.0 hours. Operational details: PULLED RIG 25M OFF LOCATION." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 80m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: PULLED OUT AND LAID DOWN CAP RUNNING TOOL. LAID DOWN 11 JOINTS OF 6 1/2' DRILL COLLAR, 1 JAR AND 9 JOINTS OF 6 5/8' HEAVY-WEIGHT DRILL PIPE." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 2.0 hours. Operational details: BACKLOADED PETROFREE MUD." "On 1993-01-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WAITED ON WEATHER FOR ANCHOR HANDLING" "On 1993-01-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: CONTINUED WAITING ON WEATHER FOR ANCHOR HANDLING" "On 1993-01-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 15.0 hours. Operational details: WAITED ON WEATHER FOR ANCHOR HANDLING" "On 1993-01-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 3.0 hours. Operational details: DE-BALLASTED RIG" "On 1993-01-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.5 hours. Operational details: CONT. DE-BALLASTING RIG." "On 1993-01-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 4.5 hours. Operational details: PULLED ANCHORS. BOLSTERED ANCHOR NO.8, 5, 4 AND 1. CONNECTED TOWING GEAR TO 'VIKING LADY'." "On 1993-01-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.5 hours. Operational details: PULLED ANCHORS. BLOSTERD ANCHOR NO. 2 AND 6." "On 1993-01-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: HAD TO STOP ANCHOR HANDLING DUE TO FAUTY TYRISTOR IN SCR. CHANGED SAME." "On 1993-01-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 2.0 hours. Operational details: PULLED ANCHORS. BLOSTERD ANCHOR NO. 3 AND PREPAIRED ANCHOR NO. 7 FOR DROP AT NEW LOCATION. ANCHOR NO. 7 HUNG OFF AT 10:25 HRS." "On 1993-02-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 4.5 hours. Operational details: RIG IN TRANSIT FROM 15/9-D3H TO 15/9-19S WITH VIKING LADY IN TOWING BRIDDLE. DROPPED ANCHOR NO 7 AT 1955 HRS" "On 1993-02-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 4.5 hours. Operational details: SET ANCHORS NO 2, 6, 3, 1 AND 5" "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 2.5 hours. Operational details: SET ANCHORS NO 8 AND 4" "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 3.5 hours. Operational details: BALLASTED RIG" "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 1.0 hours. Operational details: BALLASTED RIG TO DRILLING DRAFT" "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 4.0 hours. Operational details: TENSION-TESTED ANCHORS, RERUN ANCHOR NO 7 AND TENSION TESTED SAME TO 160 MT" "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 2.0 hours. Operational details: POSITIONED RIG OVER SLOT 3, WELL 15/9-19S" "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 7.0 hours. Operational details: RAN GUIDELINE AND CONNECTED TO HATCH. POSITIONED RIG AND OPENED HATCH. ESTABLISED GUIDELINES, ASSISTED WITH ROV." "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.5 hours. Operational details: PULLED RIG 25 M OFF LOCATION" "On 1993-02-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.5 hours. Operational details: REPAIRED TDS" "On 1993-02-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 6.0 hours. Operational details: CONT REPARING TDS" "On 1993-02-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 7.5 hours. Operational details: L/D 6 5/8' DRILLPIPE" "On 1993-02-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: PERFORMED TORQUE READING CHECK ON TDS, TESTED TORQUE AGAINST TONG LOAD CELL" "On 1993-02-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: L/D REMAINING 6 5/8' DRILLPIPE" "On 1993-02-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 7.5 hours. Operational details: P/U 5' DRILLPIPE, RACKED BACK IN DERRICK" "On 1993-02-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: CONTINUED P/U 5' DRILLPIPE" "On 1993-02-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONT P/U 5' DRILLPIPE, TOT 201 JNTS." "On 1993-02-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 14.5 hours. Operational details: WAITING ON WEATHER" "On 1993-02-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WAITING ON WEATHER" "On 1993-02-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: WAITED ON WEATHER" "On 1993-02-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WAITED ON WEATHER" "On 1993-02-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WAITED ON WEATHER" "On 1993-02-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH WITH CORROSION CAP RETRIEVING TOOL TO 86 M" "On 1993-02-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 3.5 hours. Operational details: PULLED RIG ON LOCATION, POSITIONED SAME. ENTERED CORR CAP W/RET TOOL, PULLED CAP FREE WITH 20 MT OVERPULL. PULLED RIG 25 M OFF LOCATION." "On 1993-02-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: PULLED OUT WITH CORROSION CAP." "On 1993-02-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.5 hours. Operational details: P/U AND ORIENTATED THOJ IN BOP USING CRANE" "On 1993-02-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: PREPARED BOP FOR RUNNING. INSTALLED VX-RING" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: RAN BOP STACK ON 2 EA 50 FT RISER JNTS. PRESS TESTED K/C LINES TO 345 BAR/10 MIN. CONT RIH WITH BOP/RISER. PRESS TESTED K/C 345 BAR/10 MIN" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: REPAIRED TEST PLUG FOR K/C LINES" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: PRESS TESTED K/C LINES TO 345 BAR/10 MIN." "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.0 hours. Operational details: P/U SLIP JNT AND LAND JNT, H/U K/C LINES TO SLIP JNT. INSTALLED SADLES FOR POD HOSES, INSTALLED RISER TENSIONERS. DEBALLASTED RIG 3 M. ATTEMPTED TO PRESS TEST K/C LINES." "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: CHANGED O-RING ON KILL LINE GOOSNECK, PRESS TESTED SAME TO 200 BAR" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.5 hours. Operational details: POSITIONED RIG ABOVE SLOT, BALLASTED TO DRILLING DRAFT" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: LANDED BOP OFF IN WH, CLOSED CONNECTOR. PERFORMED OVERPULL WITH 25 MT" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: L/D LANDING JNT, P/U AND INSTALL DIVERTER. H/U HYDRAULIC HOSES" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: RIH WITH TEST PLUG AND INSTALLED SAME" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: PRESS TESTED K/C LINES AND WELLHEAD CONN 345 BAR. FUNCTION TESTED BOP." "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: POOH, L/D TEST PLUG, FUNCTION TESTED SHEAR RAM WITH ACCOUSTIC" "On 1993-02-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: R/U AND RUN KOS THOJ, ADAPTER JNT AND WOR JNTS" "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: CONT RUN WOR. PRESS TEST EVERY CONNECTION 345 BAR RUN TOTAL THOJ, ADAPTER JNT AND 3 EA WOR" "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: POOH WITH WOR, ADAPTER JNT AND THOJ. L/D SAME" "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: CONT R/D KOS WOR EQUIPMENT" "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: PRESS TESTED TDS VALVES AND KELLY HOSES TO 345 BAR" "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 205m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH AND RETRIEVED BAKER RETRIEVABLE PLUG AT 205 M POOH WITH PLUG AND RET TOOL, UNABLE TO FREE PLUG FROM RET TOOL, L/D BOTH." "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3216m. The activity was categorized as 'drilling -- casing' and lasted for 7.0 hours. Operational details: M/U 8 1/2' BHA Æ19, INITIALIZED MWD MEMORY AND FUNCTION TESTED SAME. RIH AND TAGGED CMT AT 3216 M" "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3216m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: DISPLACED HOLE TO 1,40 SG PETROFREE MUD, USED 50 M3 SW AND 8 M3 HI-VISC AS SPACER" "On 1993-02-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3254m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: DRILLED CMT FROM 3216 AND RETAINER AT 3225 M, CONT DRILLING CMT TO 3254 M" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3260m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CONT DRILLING CMT FROM 3254 TO 3260 M" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: WASHED AND REAMED FROM 3260 TO RETAINER AT 3535 M" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CIRCULATED WELL FOR EVEN MUDWEIGHT IN/OUT 1,42 SG" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PRESS TESTED SURFACE LINES/KILL LINE TO 100 BAR CLOSED ANNULAR AND PRESS TESTED 9 5/8' CASING TO 62 BAR, EQUAL TO 1,71 SG" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3535m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PRESS TESTED CSG TO 62 BAR, EQUAL TO 1,71 SG" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3580m. The activity was categorized as 'drilling -- casing' and lasted for 7.0 hours. Operational details: DRILLED RETAINER AT 3535 M AND CMT TO 3480 M" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3581m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3580 TO 3581 M" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3581m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED AND CONDITIONED MUD" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3581m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: PERFORMED FIT EQUAL TO 1,71 SG MUD" "On 1993-02-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3595m. The activity was categorized as 'drilling -- drill' and lasted for 7.0 hours. Operational details: DRILLED 8 1/2' HOLE FROM 3581 TO 3595 M" "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3595m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: ATTEMPTED TO CONT DRILLING 8 1/2' HOLE, NO PROGRESS. FLOWCHECKED WELL" "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 284m. The activity was categorized as 'drilling -- trip' and lasted for 4.5 hours. Operational details: POOH FOR BIT CHANGE TO 284 M" "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONT. POOH. BROKE BIT AND BIT SUB." "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: L/D MWD-TOOL. M/U NEW MWD-TOOL." "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3576m. The activity was categorized as 'drilling -- trip' and lasted for 5.5 hours. Operational details: RE-BUILT BHA. FUNCTION TESTED MWD-TOOL. RIH TO 3576M. BROKE CIRCULATION EACH 500M." "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3595m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: LOGGED WITH THE NEW MWD-TOOL FROM 3576M TO 3595M." "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3643m. The activity was categorized as 'drilling -- drill' and lasted for 7.5 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 3595M TO 3643M." "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3643m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 1.5 hours. Operational details: CIRCULATED BU FOR SAMPLES." "On 1993-02-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3643m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: FLOW CHECKED 15 MINS. SLUGGED PIPE." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: POOH. BROKE BIT. L/D MWD AND STABILIZERS." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: M/U CORE BARREL AND CORE HEAD." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3641m. The activity was categorized as 'formation evaluation -- trip' and lasted for 6.0 hours. Operational details: P/U 2 EACH 6 1/2' DRILL COLLARS. RIH WITH BHA NO.21 TO 3641M." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3641m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP TO CHECK FOR TRIP GAS, NEGATIVE." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3641m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: SPACED OUT FOR CORING. DROPPED BALL, SEATED SAME." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3648m. The activity was categorized as 'formation evaluation -- core' and lasted for 1.5 hours. Operational details: CUT CORE NO.1 FROM 3643M TO 3648M. CORE JAMMED OFF." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 5.5 hours. Operational details: POOH. BROKE CORE HEAD." "On 1993-02-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: RECOVERED CORE." "On 1993-02-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: CONTINUED RECOVERING CORE. RACKED CORE BARREL IN DERRICK. CLEANED RIG FLOOR." "On 1993-02-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: M/U BHA NO.22. P/U MUD MOTOR AND TESTED SAME. P/U MWD-TOOL. ORIENTED NORTRAK." "On 1993-02-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1157m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: RIH TO 1157M. FILLED PIPE AND BROKE CIRCULATION EACH 500M." "On 1993-02-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3585m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: CONTINUED RIH WITH BHA NO.22 TO 3585M. FILLED PIPE AND BROKE CIRC. EACH 500M." "On 1993-02-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3648m. The activity was categorized as 'drilling -- ream' and lasted for 3.0 hours. Operational details: REAMED AND RE-LOGGED WITH MWD FROM 3585M TO 3648M." "On 1993-02-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3749m. The activity was categorized as 'drilling -- drill' and lasted for 12.0 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 3648M TO 3749M: STEERED FROM 3648M TO 3662M, 3674-3691M, 3702-3716M, 3724-3730M, 3731-3740M AND 3742-3748M." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3749m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED/ROTATED TO CLEAN HOLE." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3797m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: CONTINUED DRILLING/SURVEYING 8 1/2' HOLE TO 3797M: STEERED FROM 3763 TO 3767M AND 3769M TO 3779M." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3873m. The activity was categorized as 'drilling -- drill' and lasted for 11.0 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 3797M TO 3873M: STEERED FROM 3797M TO 3799M AND FROM 3815M TO 3827M. ATTEMPTED STEERING AT 3869M, NEGATIVE AS MOTOR STALLED OUT. USED 50 TONS OVERPULL TO FREE PIPE AFTER ATTEMPTING TO STEER." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3873m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED TO CLEAN HOLE." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3546m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: WIPER TRIP TO 3546M. ROTATED PIPE IN SLIPS ON FIRST 8 CONNECTIONS DUE TO TENDENCIES OF STICKING. NO TIGHT HOLE." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3546m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: SLIPPED AND CUT 32M DRILL LINE." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3873m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: RAN IN TO 3873M, NO FILL." "On 1993-03-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3877m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 3873M TO 3877M. STEERED FROM 3875M TO 3876M." "On 1993-03-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3894m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 3877M TO 3894M. ATTEMPTED STEERING AT 3877M, NEGATIVE DUE TO MOTOR STALLING OUT." "On 1993-03-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3950m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 3894M TO 3950M. NO STEERING." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3955m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: CONT. ROTATION DRILLING/SURVEYING TO 3955M." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3955m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED B/U AND SHAKERS CLEAN." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3955m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: FLOW CHECKED. PUMPED SLUG. POOH FOR BIT CHANGE TO 3528M." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1200m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONT. POOH TO 1200M." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1200m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: FOUND MOTOR ON UPPER RACKING ARM LOOSE. REPAIRED SAME." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: CONT. POOH. BROKE BIT. L/D MWD TOOL, MOTOR, STABILISERS AND X-OVERS" "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: M/U BHA NO. 23 AND RIH TO 800M. TESTED MWD-TOOL. AT 800M, GOT ALARM ON LOW OIL PRESSURE ON TOP DRIVE." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 5.0 hours. Operational details: TOOK DOWN OIL PUMP ASSEMBLY TO REPAIR SAME." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: FUNCTION TESTED BOP ON YELLOW POD. TESTED ACOUSTIC SYSTEM." "On 1993-03-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: CONTINUED REPAIRING TDS: CHANGED OUT OIL PUMP." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: CONT. REPAIRING TDS. RE-INSTALLED OIL PUMP ASSEMBLY." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 800m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: FILLED PIPE. BROKE CIRCULATION AND CIRCULATED A RISER VOLUME." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3028m. The activity was categorized as 'drilling -- trip' and lasted for 3.5 hours. Operational details: CONT. RIH TO 3028M. FILLED PIPE AND BROKE CIRC. EACH 500M." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3565m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONT. RIH WITH BHA NO.23 TO 3565M." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3565m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED TO CONDITION MUD" "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3884m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONT. RIH TO 3884M, TOOK WEIGHT." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3955m. The activity was categorized as 'drilling -- ream' and lasted for 3.5 hours. Operational details: WASHED/REAMED TIGHT HOLE FROM 3884M TO 3955M." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3971m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: ROTARY DRILLED AND SURVEYED 8 1/2' HOLE FROM 3955M TO 3971M." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3955m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RE-LOGGED WITH MWD-TOOL FROM 3941M TO 3955M." "On 1993-03-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4083m. The activity was categorized as 'drilling -- drill' and lasted for 10.0 hours. Operational details: CONTINUED DRILLING/SURVEYING 8 1/2' HOLE FROM 3971M TO 4083M." "On 1993-03-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4140m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONT. DRILLING/SURVEYING 8 1/2' HOLE TO 4140M." "On 1993-03-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4298m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: CONTINUED DRILLING/SURVEYING 8 1/2' HOLE FROM 4140M TO 4298M. FLOW CHECKED AT 4239M DUE TO DRILLING BREAK, NEGATIVE." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4308m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: CONT. DRILLING/SURVEYING 8 1/2' HOLE TO 4308M. FLOW CHECKED AT 4303M AND AT 4308M DUE TO DRILLING BREAKS, NEGATIVE." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4308m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED DUE TO HIGH ROP." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4328m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 4308M TO 4328M." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4328m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP FOR SAMPLE." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4328m. The activity was categorized as 'formation evaluation -- circulation samples' and lasted for 0.5 hours. Operational details: CIRCULATED BOTTOMS UP FOR SAMPLES." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4328m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: FLOWCHECKED FOR 15 MIN,NEGATIVE. PUMPED SLUG." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: POOH TO SHOE.WORKED TIGHT SPOT AT 3662M WITH MAX 30 TON OVERPULL." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: FLOW CHECKED, NEGATIVE." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2173m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH TO 2173M." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2173m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: REPAIRED UPPER RACKING ARM." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 700m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: CONTINUED POOH TO 700M." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 700m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: RAPAIRED UPPER RACKING ARM." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: CONTINUED POOH.LAID DOWN MONEL,STABILIZERS AND MWD TOOL." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: PICKED UP CBBL AND INSTALLED 27M ALUMINIUM INNER BARREL. SPACED OUT CBBL AND MADE UP COREHEAD." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3550m. The activity was categorized as 'formation evaluation -- trip' and lasted for 5.0 hours. Operational details: RIH WITH BHA NO. 24 TO 3550M. BROKE CIRCULATION EACH 600M." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3550m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED TO CONDITION MUD." "On 1993-03-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4298m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.5 hours. Operational details: CONTINUED RIH FROM 3550M TO 4298M." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4328m. The activity was categorized as 'formation evaluation -- trip' and lasted for 1.0 hours. Operational details: BROKE CIRCULATION. WASHED/REAMED TO 4328M." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4328m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4328m. The activity was categorized as 'formation evaluation -- trip' and lasted for 0.5 hours. Operational details: DROPPED BALL, DISPLACED AND SEATED SAME." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- core' and lasted for 3.0 hours. Operational details: CUT CORE NO.2 FROM 4328M TO 4338M." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4355m. The activity was categorized as 'formation evaluation -- core' and lasted for 4.5 hours. Operational details: CONTINUED CUTTING CORE NO.2 FROM 4338M TO 4355M." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4355m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: CIRCULATED 10 MINS. FLOW CHECKED 15 MINS, NEGATIVE. PUMPED SLUG." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 29m. The activity was categorized as 'formation evaluation -- trip' and lasted for 6.0 hours. Operational details: POOH TO 9 5/8' CASING SHOE. FLOW CHECKED, NEGATIVE. CONTINUED POOH TO 29M, FLOW CHECKED AT 500M, NEGATIVE." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 29m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: PREPARED FOR RECOVERING CORE.RECORDED 650 PPM H2S GAS FROM TOP OF COREBARREL. SOUNDED GENERAL ALARM AND ORDERED ALL ESSENTIAL PERSONNEL TO PORT BOX GIRDER FORWARD. EQUIPPED DRILL-FLOOR PERSONNEL WITH BREATHING APPARATUS. CLOSED SHEAR RAM TO MONITOR WELL ON CHOKE. CARRIED OUT H2S MEASUREMENTS ON RIG FLOOR." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: HELD SAFETY/PRE-OPERATION MEETING WITH INVOLVED PERSONNEL." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: INSTALLED LIFT SUB. PULLED OUT INNER BARREL, KEPT SAME HANGING IN TUGGER LINE FOR VENTING OUT H2S." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: RAN BACK IN WITH INNER BARREL. DRILLED 6MM DIAMETER VENT HOLES EACH METER. MEASURED H2S LEVELS WHILE DRILLING. PULLED INNER BARREL OUT AFTER DRILLING VENT HOLES." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: KEPT INNER BARREL HANGING IN TUGGER LINE FOR VENTING WHILE MEASURING H2S-LEVELS. ALLOWED PERSONNEL TO GO BACK INDOOR." "On 1993-03-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: HELD SAFETY MEETING WITH INVOLVED PERSONNEL PRIOR TO L/D CORE BARRELS." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: L/D INNER BARRELS. SECURED AREA AROUND BARRELS. BROKE CORE HEAD." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: OPENED CHOKE. CIRCULATED DOWN KILL LINE, UP CHOKE LINE THROUGH POORBOY DEGASSER." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: OPENED SHEAR RAM. FLOW CHECKED, NEGATIVE. CIRCULATED A RISER VOLUME DOWN K/C-LINES, NO GAS/H2S." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: VERIFIED RIG FLOOR/SURROUNDINGS H2S-FREE. BLEW RIG AIR INTO/THROUGH RELEVANT CAVITIES TO CLEAR EVENTUAL H2S. FINISHED THE USE OF BREATHING APPARATUS ON THE RIG FLOOR/SHAKER ROOM." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: MADE UP CORE BARREL WITH 27M ALUMINIUM INNER TUBES. SPACED OUT INNER BARREL AND MADE UP CORE HEAD." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3548m. The activity was categorized as 'formation evaluation -- trip' and lasted for 5.0 hours. Operational details: RIH WITH CORE BARREL TO 3548M. BROKE CIRCULATION EACH 600M." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3548m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRCULATED TO CONDITION MUD. INSTALLED MUD SAVER SUB ON DRILLING STAND" "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4326m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: CONTINUED RIH TO 4326M." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4355m. The activity was categorized as 'drilling -- ream' and lasted for 0.5 hours. Operational details: REAMED FROM 4326M TO 4355M." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4355m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATED BOTTOMS UP." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4355m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.5 hours. Operational details: DROPPED BALL. DISPLACED AND SEATED SAME. TOOK S.C.R." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4383m. The activity was categorized as 'formation evaluation -- core' and lasted for 5.0 hours. Operational details: CUT CORE NO. 3 FROM 4355M TO 4383M." "On 1993-03-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4134m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: CIRCULATED 15 MINUTES. FLOW CHECKED, NEGATIVE. SLUGGED PIPE. POOH WITH CORE BARREL TO 4134M." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3555m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: CONT. POOH WITH CORE BARREL TO 3555M. WORKED TIGHT SPOT AT 3670M." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1667m. The activity was categorized as 'formation evaluation -- trip' and lasted for 3.5 hours. Operational details: FLOW CHECKED IN 9 5/8' CASING SHOE, NEGATIVE. CONT. POOH TO 1667M." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1667m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: RE-ARRANGED SET-BACK IN DERRICK." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 717m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.0 hours. Operational details: CONTINUED POOH WITH CORE NO.3 TO 1260M. MONITORED 11 PPM H2S INSIDE THE PIPE. PREPARED H2S EQUIPMENT. CONTINUED POOH TO 717M. H2S IN PIPE FROM 9 PPM TO 17 PPM." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: INSTALLED MAERSK H2S SAFETY EQUIPMENT ON RIG FLOOR." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- trip' and lasted for 2.5 hours. Operational details: CONTINUED POOH FROM 717M. MEASURED H2S-LEVELS ON THE DRILL FLOOR AND IN THE PIPE: NO H2S DETECTED ON DRILL FLOOR, BETWEEN 6 PPM AND 15 PPM IN THE PIPE. PIPE CAME WET AT 545M, NO H2S DETECTED THEREAFTER. PREPARED BREATHING APPARATUS. PULLED CORE BARREL TO SURFACE. BROKE CORE HEAD. NO H2S." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: L/D INNER BARREL. RACKED OUTER BARREL IN DERRICK. RECOVERED 28,15M CORE,100%" "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: M/U SPRING LOADED BOP TEST TOOL AND RIH TO 105M." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.5 hours. Operational details: TESTED BOP ON BLUE POD: TESTED RAMS AND LAP TO 20/345 BAR FOR 5/10 MIN AND UAP TO 20/240 BAR FOR 5/10 MIN. FUNCTIONTESTED ON YELLOW POD." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: ATTEMPTED FUNCTIONING UPR AND MPR WITH ACOUSTIC FROM THE BRIDGE, GOT ERRATIC RESPONSE/NO VERIFICATION OF OPERATION. VERIFIED CLOSED RAMS BY OPENING SAME FROM THE KOOMEY UNIT." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: FUNCTIONED UPR AND MPR WITH ACOUSTIC SYSTEM FROM CELLAR DECK, OK." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: POOH WITH SPRING LOADED TOOL. L/D SAME." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: PRESSURE TESTED STAB-IN VALVE, TDS INSIDE BOP'S, KELLY HOSE AND STANDPIPE VALVE TO 20/345 BAR, 5/10 MINS." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: M/U 8 1/2' BIT AND TRIPLE COMBO MWD-TOOL." "On 1993-03-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: ATTEMPTED TESTING MWD-TOOL, NEGATIVE: LOSS OF CONTACT IN JUNCTION BOX FOR TEST CABLE. REPAIRED SAME." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: TESTED MWD. INSTALLED RADIOACTIVE SOURCE." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3144m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: CONTINUED M/U BHA NO.26 AND RIH TO 3144M. FILLED PIPE/BROKE CIRCULATION EACH 600M." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3560m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONT. RIH WITH 8 1/2' ROTARY ASSEMBLY TO 3560M. FILLED PIPE AND BROKE CIRCULATION EACH 600M." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3560m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED TO CONDITION MUD." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3608m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONT. RIH TO 3608M." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3655m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: LOGGED WITH TRIPLE COMBO MWD-TOOL FROM 3608M TO 3655M." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4297m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONT. RIH TO 4297M. FILLED PIPE." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4383m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.5 hours. Operational details: BROKE CIRCULATION. LOGGED WITH MWD-TOOL FROM 4313M TO 4383M." "On 1993-03-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4453m. The activity was categorized as 'drilling -- drill' and lasted for 8.5 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 4383M TO 4453M. FLOW CHECKED AT 4392M AND 4415M, NEGATIVE." "On 1993-03-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4503m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: CONTINUED DRILLING/SURVEYING 8 1/2' HOLE FROM 4453M TO 4503M. FLOW CHECKED AT 4487M, NEGATIVE." "On 1993-03-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4527m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 4503M TO 4527M." "On 1993-03-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4527m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED HOLE CLEAN DUE TO HIGH TORQUE AND POOR HOLE CLEANING." "On 1993-03-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4641m. The activity was categorized as 'drilling -- drill' and lasted for 14.0 hours. Operational details: DRILLED/SURVEYED 8 1/2' HOLE FROM 4527M TO TD AT 4641M." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4641m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.0 hours. Operational details: CIRCULATED HOLE CLEAN. FLOW CHECKED, NEGATIVE." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3672m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: POOH TO 3672M FOR WIPER TRIP TO 9 5/8' CASING SHOE. WORKED TIGHT SPOT AT 3672M. MAX 30 TON OVERPULL." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3546m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: CONTINUED POOH FROM 3672M TO 3546M." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3546m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: INSTALLED CIRCULATING EQUIPMENT AND CIRCULATED AT 3650M. CIRCULATED WITH 46 SPM AND 50 BAR." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3650m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: SLIPPED AND CUT DRILL LINE." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4612m. The activity was categorized as 'drilling -- ream' and lasted for 3.0 hours. Operational details: RIGGED DOWN CIRCULATION EQUIPMENT. RIH AND WORKED TIGHT SPOTS FROM 3650M TO 3656M AND FROM 3664M TO 3670M. RIH TO 4612M," "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4641m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.5 hours. Operational details: BROKE CIRCULATION AND TAGGED BOTTOM AT 4641M. CIRCULATED HOLE CLEAN." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3546m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: POOH FROM 4641M TO 3546M AND FLOW CHECKED 15 MIN." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3546m. The activity was categorized as 'drilling -- trip' and lasted for 7.5 hours. Operational details: POOH. LAID DOWN MWD TOOL AND STABS. LAID DOWN CORE BARREL FROM DERRICK." "On 1993-03-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: RIGGED UP ATLAS WIRELINE." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: FINISHED RIGGING UP ATLAS WIRELINE." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4615m. The activity was categorized as 'formation evaluation -- log' and lasted for 4.5 hours. Operational details: RAN LOG NO 1. DIFL/AC/ZDL/CN/GR/CHT. IN AT 01:45 HRS." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4488m. The activity was categorized as 'formation evaluation -- log' and lasted for 3.0 hours. Operational details: CONTINUED LOG RUN NO 1. TO 9 5/8' SHOE. RIH TO 3725M. LOGGED REPEAT SECTION FROM 3725M TO 3697M. UNABLE TO PASS 3697M. TOP OF TOOL AT 3664.5M." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3664m. The activity was categorized as 'formation evaluation -- other' and lasted for 3.5 hours. Operational details: MADE SEVERAL ATTEMTS TO FREE STUCK LOGGING TOOLS BY WORKING CABLE WITH MAX 6000 LBS OVERPULL. KEPT CABLE IN TENSION WHILE WORKING CALIPER ARM." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3697m. The activity was categorized as 'interruption -- fish' and lasted for 4.5 hours. Operational details: RIGGED DOWN ATLAS WIRELINE EQUIPMENT ON RIG FLOOR. INSTALLED T-BAR IN ROTARY AND CUT CABLE 5M ABOVE RKB. PREPAIRED AND MADE UP CATCHER, ATTACHED SAME AND PERFORMED PULLTEST. INSTALLED TOP SHEAVE AT CROWN. MADE UP OVER SHOT TO 5' HWDP." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 57m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: FEAD CATCHER THROUGH DP AND RIH WITH OVER SHOT ASSEMBLY." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 57m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: HAD PROBLEMS WITH GEAR BOX ON ATLAS WIRELINE UNIT." "On 1993-03-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 804m. The activity was categorized as 'interruption -- fish' and lasted for 5.0 hours. Operational details: CONTINUED RIH WITH OVERSHOT ASSEMBLY TO 804M." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2100m. The activity was categorized as 'interruption -- fish' and lasted for 6.0 hours. Operational details: CONTINUED RIH WITH OVERSHOT ASSEMBLY TO 2100M. BROKE CIRCULATION AND RETERMINATED CATCHER AT 1200M." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3530m. The activity was categorized as 'interruption -- fish' and lasted for 6.5 hours. Operational details: CONTINUED RIH WITH OVERSHOT TO 3530M. BROKE CIRCULATION AND CHECKED CABLE HEAD AT 2400M AND 3530M." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3530m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: MADE UP PUMP-IN SUB AND STUFFING BOX ASSY ON A STAND AND RACKED SAME BACK IN DERRICK. PICKED UP ONE SINGLE FOR SPACE OUT." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3656m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: CONTINUED RIH WITH OVERSHOT TO 3656M." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3656m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: MADE UP CIRCULATION STAND. INSTALLED INSERTS FOR STUFFING BOX AND RIGGED UP CIRCULATION HOSE." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3675m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: BROKE CIRCULATION WITH 7 SPM AND 23 BAR. RIH AND ENGAGED FISH AT 3675M. PULLED BACK 3M TO ENSURE ENGAGEMENT OF FISH. POOH TO 3512M. BOTTOM OF FISH AT 3545,5M." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3512m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: WHILE REPLACING TRANSMISSION ON ATLAS UNIT: TENSIONED UP, RETERMINATED AND LANDED CABLE IN DRILL PIPE. SLUGGED PIPE." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3512m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: PREPARED TO BREAK WEAK POINT ON CABLE HEAD. LATCHED T-BAR IN ELEVATOR AND PULLED CABLE FREE WITH 5 TON OVERPULL." "On 1993-03-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3512m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: CONNECTED CABLE ENDS TOGETHER TO PULL CABLE OUT OF HOLE." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3512m. The activity was categorized as 'interruption -- fish' and lasted for 1.0 hours. Operational details: PULLED CABLE OUT OF HOLE. ( CABLE BROKE AT WEEKPOINT AS INTENDED.)" "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3512m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: RIGGED DOWN ATLAS WIRELINE AND PREPARED TO POOH WITH DRILLPIPE." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 900m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: POOH WITH OVERSHOT AND LOGGING TOOLS FROM 3512M TO 900M." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 1.5 hours. Operational details: CONTINUED POOH WITH OVERSHOT AND LOGGING TOOLS." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 2.0 hours. Operational details: RECOVERED TOOLSTRING FROM OVERSHOT. REMOVED RADIOACTIVE SOURCES AND LAID DOWN LOGGING TOOLS." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: RIGGED DOWN ATLAS WIRELINE, RE-ARRANGED SET-BACK AND CLEARED RIG FLOOR." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4630m. The activity was categorized as 'drilling -- casing' and lasted for 7.0 hours. Operational details: MADE UP 8 1/2' CLEAN-OUT ASSEMBLY AND RIH TO 4630M. BROKE CIRCULATION AND FILLED PIPE EVERY 850M." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4641m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: BROKE CIRCULATION. TAGGED BOTTOM AT 4641M, CIRCULATED AND CONDITIONED MUD PRIOR TO POOH, TO RUN 7' LINER." "On 1993-03-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4515m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH TO RUN 7' LINER." "On 1993-03-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4515m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: CONTINUED POOH. REAMED TIGHT SPOT AT 4515M, 4454M AND 4415M. WITH MAX 30 TONN OVERPULL. HAD PROBLEMS WITH STALLING ROTARY. RIH TO TD AT 4641M." "On 1993-03-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4408m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: BACKREAMED OUT OF HOLE FROM 4641M TO 4408M. HAD TO WORK TIGHT SPOT AT 4415M." "On 1993-03-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4408m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: WORKED TIGHT SPOT AT 4408M WHEN SCR'S FOR TOP DRIVE FAILED. CIRCULATED AND WORKED STRING WHILE TROUBLESHOOTING SCR SYSTEMS. UNABLE TO PASS 4408M." "On 1993-03-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 7.0 hours. Operational details: CONTINUED BACKREAMING OUT OF HOLE FROM 4408M TO 3569M." "On 1993-03-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CIRCULATED BTM'S UP. FLOWCHECKED, NEGATIVE." "On 1993-03-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 8.5 hours. Operational details: PULLED OUT OF HOLE FORM 3569M. STRAPPED AND DRIFTED PIPE WHILE POOH." "On 1993-03-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: MADE UP CEMENT STAND AND RACKED SAME BACK IN DERRICK. RIGGED UP TO RUN 7' CASING." "On 1993-03-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: FINISHED RIGGING UP 7' CASING HANDLING EQUIPMENT. HELD PRE-JOB MEETING WITH CREW." "On 1993-03-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 351m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: RAN SHOE JOINT, INTERNEDIATE JOINT AND FLOAT COLLAR JOINT. CHECKED FLOAT, INSTALLED LANDING COLLAR. TREAD LOCKED FIRST THREE CONNECTIONS. RAN 31 JOINTS OF 7' CASING TO 351M. FILLED CASING WITH 1,40 S.G. MUD EVREY 5 JOINTS WHILE RIH." "On 1993-03-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1441m. The activity was categorized as 'drilling -- casing' and lasted for 11.0 hours. Operational details: CONTINUED RUNNING 7' CASING TO 1441M. FILLED CASING WITH 1,40 S.G. MUD EVERY 5 JOINTS WHILE RIH." "On 1993-03-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1441m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: INSTALLED CEMENT PLUGS ONTO LINER HANGER AND MADE UP HANGER TO 7' CASING." "On 1993-03-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1441m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CIRCULATED 7' LINER VOLUME PRIOR TO RUNNING." "On 1993-03-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2587m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: RIH WITH LINER TO 2587M. FILLED PIPE WITH 1,40 S.G. MUD EVERY 3 STANDS AND BROKE CIRCULATION EVERY 6 STANDS." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: CONTINUED RIH WITH LINER TO 3569M. FILLED PIPE WITH 1,40 S.G. MUD EVERY 3 STANDS AND BROKE CIRCULATION EVERY 6 STANDS." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3569m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CIRCULATED AT CASING SHOE TO ESTABLISH MAX RATE BEFORE RUNNING INTO OPEN HOLE. MAX RATE 453 LTR AT 60 BAR. RECORDED UP AND DOWN WEIGHT." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3809m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CONTINUED RIH WITH LINER TO 3809M. FILLED PIPE AND BROKE CIRCULATION WITH 1,40 S.G. MUD EVERY 3 STANDS." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4630m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONTINUED RIH WITH 7' LINER TO 4630M. FILLED PIPE AND BROKE CIRCULATION WITH 1,40 S.G. MUD EVERY 3 STANDS." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4641m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: BROKE CIRCULATION AND TAGGED BOTTOM AT 4641M. PICKED UP 1M." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4640m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: DROPPED SETTING BALL AND CHASED SAME WITH RIG PUMPS. SET LINER HANGER WITH 150 BAR. SHEARED OUT BALLSEAT WITH 185 BAR." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4640m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: CIRCULATED AND CONDITIONED MUD PRIOR TO CEMENT JOB. ROTATED LINER 20 RPM WHILE CIRCULATING. MAX TORQUE AT START OF ROTATION: 32540 NM (24000 FTLBS). MAX TORQUE DURING CIRCULATION: 23050 NM (17000 FTLBS). CIRCULATED WITH MAX 1400 LPM." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4640m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIGGED UP CEMENT HOSE. PUMPED 15 M3 SPACER WITH RIG PUMPS. PRESSURE TESTED SURFACE LINES TO 350 BAR. DROPPED DART FOR BOTTOM PLUG." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4640m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: MIXED AND PUMPED 30,5 M3 1.90 S.G. CEMENT. DROPPED DART FOR TOP PLUG. PUMPED 1,5 M3 SPACER USING RIG PUMPS." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4640m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: DISPLACED CEMENT WITH 53,7M3 1,40 SG MUD USING RIG PUMPS. PLUG DID NOT BUMP. ROTATED LINER WITH 40 RPM, REDUCED TO 20 RPM TOWARDS END OF DISPLACEMENT. MAX TORQUE WHILE DISPLACING CMT: 24400 NM (18000 FTLBS). NO BACKFLOW." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2906m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RELEASED LINER RUNNING TOOL, NO BACKPRESSURE/BACKFLOW. PULLED OUT OF HOLE FROM 3203M TO 2906M." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2906m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CIRCULATED BOTTOMS UP. TRACES OF SPACER IN RETURNS." "On 1993-03-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1470m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH WITH LINER RUNNING TOOL FROM 2906M TO 1470M." "On 1993-03-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: POOH WITH LINER RUNNING TOOL FROM 1470M TO SURFACE. LAID DOWN 78 JOINTS OF 5' DP WHILE POOH." "On 1993-03-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: LAID DOWN NODECO HANGER RUNNING TOOL AND CEMENT STAND." "On 1993-03-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2870m. The activity was categorized as 'drilling -- casing' and lasted for 7.5 hours. Operational details: MADE UP 8 1/2' BIT AND SCRAPER AND RIH TO 2870." "On 1993-03-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3206m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: WASHED AND REAMED FROM 2870M TO TOP OF PBR AT 3206M, NO HARD CEMENT." "On 1993-03-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3206m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRCULATE BOTTOMS UP, NO TRACES OF CEMENT." "On 1993-03-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 827m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: SLUGGED PIPE AND POOH FROM 3206M TO 827M. LAID DOWN 14 JOINTS OF 5' DP WHILE POOH." "On 1993-03-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: CONTINUED POOH FROM 827M TO SURFACE, BROKE BIT AND SCRAPER. LAID DOWN 49 JOINTS 5' DRILLPIPE WHILE POOH." "On 1993-03-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CHANGED TO SLIMHOLE HANDLING EQUIPMENT, PICKED UP 2 JOINTS 4 3/4' DRILL COLLARS AND MADE UP 6' BIT AND SCRAPER." "On 1993-03-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: TESTED LINER LAP TO 70 BAR/10 MIN." "On 1993-03-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 90m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CONTINUED MAKING UP 6' BHA AND PICKED UP 3 1/2' DRILL PIPE WHILE RIH TO 90M." "On 1993-03-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4270m. The activity was categorized as 'drilling -- casing' and lasted for 16.0 hours. Operational details: PICKED UP 137 JOINTS 3 1/2' DRILLPIPE, PBR MILL AND TOPDRESS MILL, 9 5/8' CASING SCRAPER WHILE RUNNING IN HOLE FROM 90M TO 4270M" "On 1993-03-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4305m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: WORKED AREA FROM 4270M TO 4305M WITH 7' CASING SCRAPER ROTATING AT 66 RPM WITH 22000 NM TORQUE AND PUMPING WITH 890 LPM AT 54 BAR." "On 1993-03-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4523m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: WASHED DOWN FROM 4300M AND TAGGED TOP OF CEMENT AT 4523M. WASHING WITH 190 LPM, 110 BAR AND 60 RPM." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4523m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED WELL PRIOR TO DRILLING EXCESS CEMENT IN LINER, DUE TO HIGH CIRCULATION PRESSURES." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4529m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: DRILLED EXCESS SEMENT IN 7' LINER FROM 4523M TO 4529M." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4529m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: FIRST ROUND CIRCULATION ARRIVED AT SURFACE, AND IT WAS SO THICK IT MADE THE SHAKER TRAYS OVERFLOW. CLEANED SHAKERS FROM THICK MUD." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4529m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: FINISHED CLEANING SHAKERS AND FLOW LINE OF THICK MUD." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4529m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: CIRCULATED REMAINDER OF THICK MUD OUT OF WELL UNTIL SURFACE SYSTEMS WERE OPERATING PROPERLY." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4588m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: DRILLED EXCESS CEMENT IN 7' LINER FROM 4529M TO 4588M." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4607m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: DRILLED EXCESS CEMENT IN 7' LINER FROM 4588M TO 4607M." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4607m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: TAGGED LINER PBR AT 3207M, (HAD CIRCULATION PRESSURE INCREASE OF 5 BAR AND TORQUE INCREASE OF 7400 - 8900 NM) AND DRESSED OFF TOP OF PBR." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4607m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: CIRCULATED WELL CLEAN. TOOK UP/DOWN WEIGHTS AND TORQUE READINGS." "On 1993-03-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2241m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: SLUGGED PIPE AND POOH FROM 4607M TO 2241M." "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: CONTINUED POOH FROM 2241M TO SURFACE. LAID DOWN SCRAPERS, PBR MILL, TOPDRESS MILL, JUNK BASKET AND BROKE BIT WHILE POOH. NOTHING IN JUNK BASKET. NB!! FLOAT MISSING ON FLOOR !!NB" "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.0 hours. Operational details: RIGGED UP TO RUN GR/CCL/CBL/VDL, RIGGED DOWN SAME DUE TO DRILL PIPE FLOAT FALLING INTO WELL." "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: CIRCULATED KILL/CHOKE LINES AND CYCLE RAMS ON BOP WHILE PREPARING TO RUN CCL/JUNKBASKET/GAUGERING." "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 3.5 hours. Operational details: RIH WITH CCL/JUNK BASKET/ GAUGERING, EXPERIENCED TOOL FAILURE AT 1000M. POOH AND ATTEMPTED TO LOCATE AND REPAIR FAILURE. RIGGED DOWN ATLAS WIRELINE." "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: MADE UP PBR AND TOP DRESS MILL (DRESSED WITH TUBE-LOCK ON MILL SURFACES), PICKED UP 3 JOINTS 6 1/2' DRILL COLLARS AND RIH TO 2770M." "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: RE-RACKED 3 1/2' DRILL PIPE IN DERRICK." "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3207m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: CONTINUED RIH AND HAD A SINGLE POINT OF TORQUE INCREASE FROM 5200NM TO 9600NM AT 3205M, BEFORE HITTING LINER TOP AT 3207M. HIT TOP OF LINER AT 3207M, (HAD TORQUE INCREASE FROM 5200NM TO 7400NM) AND DRESSED SAME WITH MAX TORQUE 11000NM." "On 1993-03-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3207m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: STARTED CIRCULATING BOTTOMS UP." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3207m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: FINISHED CIRCULATING BOTTOMS UP." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: SLUGGED PIPE AND POOH. LAID DOWN 24 JOINTS OF 5' DRILL PIPE WHILE POOH." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: BROKE PBR AND TOP DRESS MILL. TUBELOCK WAS GONE, THIS INDICATES THAT IT WAS ENGAGED WITH TOP OF LINER." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4540m. The activity was categorized as 'formation evaluation -- log' and lasted for 9.5 hours. Operational details: LOGGED CBL/VDL/GR/CCL FROM 4540M TO 3150M. RIH AT 07:50 HRS, OOH AT 1600 HRS." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: TESTED CASING/LINER LAP TO 147 BAR / 15 MIN. WHILE RIGGED DOWN CBL/VDL/GR/CCL AND RIGGED UP TO RUN VSP/GR." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: RIH WITH VSP/GR TO 1000M." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: REPAIRED HYDRAULIC LEAK ON ATLAS UNIT." "On 1993-03-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3924m. The activity was categorized as 'formation evaluation -- log' and lasted for 2.5 hours. Operational details: CONTINUED RIH WITH VSP FROM 1000M TO 3924M." "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4580m. The activity was categorized as 'formation evaluation -- log' and lasted for 6.0 hours. Operational details: CONTINUED RIH WITH VSP FROM 3924M TO 4580M. TOOK VSP SHOTS FROM 4580M TO 1294M." "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1294m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.0 hours. Operational details: FINISHED LOGGING VSP LOG AND POOH." "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 1.5 hours. Operational details: RIGGED DOWN VSP TOOLS AND RIGGED UP GYRO TOOLS." "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4540m. The activity was categorized as 'formation evaluation -- log' and lasted for 8.0 hours. Operational details: RAN GYRO SURVEY FROM 4540M TO 3503M." "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- log' and lasted for 0.5 hours. Operational details: RIGGED DOWN ATLAS WIRELINE." "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: SLIPPED AND CUT 32M DRILL LINE." "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: RAN IN HOLE TO 1000M AND SWEPT HOLE WITH: 9M3 LOW REOLOGY PETROFREE MUD FOLLOWED BY 10M3 ESTER AND 50M3 SEAWATER. OBSERVED WELL ON TRIP TANK 30MIN. POOH" "On 1993-03-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.5 hours. Operational details: MADE UP JETSUB AND WASHED RISER AND BOP WHILE RIH TO WELLHEAD. WASHED ACROSS BOP/WELLHEAD AREA SEVERAL TIMES WITH 3500LPM AND 30RPM. FLUSHED DOWN KILL/CHOKE LINES WHILE CYCLED ALL BOP CAVITIES. DISPLACED HOLE UNTIL RETURNS WERE CLEAN." "On 1993-03-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 106m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: SWEPT HOLE WITH 5M3 ESTER FOLLOWED BY 5M3 DETERGENT PILL, 15M3 SEAWATER, 5M3 DETERGENT PILL (500LPM) AND SEA WATER (3500LPM/30RPM) UNTIL NTU READINGS WERE THE SAME IN AND OUT (NTU=60). WASHED RISER AGAIN WHILE POOH." "On 1993-03-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: HAD TO CHANGE 3 1/2' ELEVATORS. THE ELEVATORS THAT WERE MOUNTED DID NOT WORK." "On 1993-03-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 173m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: STARTED RIH WITH 3 1/2' DRILLPIPE, COULD NOT FIND A X-OVER NEEDED TO PUT 7' SCRAPER IN THE MIDDLE OF THE 3 1/2' DRILL PIPE. POOH. (X-OVER 3 1/2'IF PINN X 4 1/2'FULL-HOLE PINN)" "On 1993-03-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1027m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: PICKED UP 7' CASING SCRAPER AND RIH WITH 3 1/2' DRILL PIPE TO 1072M." "On 1993-03-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1072m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.5 hours. Operational details: TESTED SURFACE LINES AGAINST FAILSAFE TO 345 BAR / 5 MIN. TESTED CASING / LINER LAP AGAINST UPPER PIPE RAM TO 345 BAR / 15 MIN." "On 1993-03-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4572m. The activity was categorized as 'drilling -- drill' and lasted for 12.0 hours. Operational details: CONTINUED RIH FROM 1072M TO 4572M. SPACED OUT AND PICKED UP PBR PACKER ON THE WAY IN." "On 1993-03-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4572m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: ESTABLISHED CIRCULATION AND STUNG INTO LINER. SET PBR PACKER AND RELEASED RUNNING TOOL. PULLED OUT 10M AND PAINTED MARKER ON PIPE TO MARK LOWEST RECIPROCATING POINT." "On 1993-03-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: PULLED OUT TO 4133M, WORKED AREA FROM 4133M TO 4103M WITH SCRAPER AND RAN BACK IN HOLE TO 4562M. WORKED SCRAPER BY RECIPROCATING AND ROTATING 30 RPM. (TORQUE READINGS: 21000NM WHILE PULLING AND 15000NM WHILE RUNNING IN.)" "On 1993-03-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4562m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 4.0 hours. Operational details: SWEPT WELL WITH 15 M3 ESTER, 10 M3 DETERGENT PILL AND SEA WATER BY REVERSE CIRCULATION. (HOLDING BACKPRESSURE ON SURFACE TO MAINTAIN CONSTANT BOTTOM HOLE PRESSURE) PUMPED AT 40 SPM, 175 BAR AND FINAL VALUES WERE 40 SPM 277 BAR." "On 1993-03-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4562m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 2.0 hours. Operational details: CONTINUED REV CIRCULATION. FINAL SHUT IN PRESS WHEN STOPPED PUMPING 93 BAR. BLEED OFF PRESS IN STEPS TO TEST LINER/PBR NEGATIVE. OBSERVED WELL ON TRIP TANK FOR 30 MIN." "On 1993-03-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4562m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 16.0 hours. Operational details: PERFORMED TORQUE READINGS. PUMPED 10 M3 DETERGENT PILL FOLLOWED BY 15 M3 SEA WATER, REPEATED OPERATION THREE TIMES. CONT PUMPING 10 M3 FLOCCULANT PILL FOLLOWED BY SEAWATER. FINAL NTU READING 90 NTU. PUMPED 6 M3 SW, 6 M3 DETERGENT PILL FOLLOWED BE SW. ALL PILLS IN RETURN WERE ROUTED BACK TO SLOP PIT. FINAL NTU READING 80 NTU." "On 1993-03-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4262m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: PUMPED 4,5 M3 1,36 SG CACL2 BRINE, DISPLACED SAME WITH 30.9 M3 SEA WATER TO PLACE THE BALANCED BRINE PILL." "On 1993-03-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4340m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 4.5 hours. Operational details: POOH FROM 4562 TO 4340 M. DISPLACED WELL TO 1,15 SG NACL BRINE. LOST APPROX 65 M3 1,15 SG BRINE TO SEA DUE TO OPEN DRAIN VALVE IN CMT UNIT. NTU READING ON NACL IN RETURN: 52 NTU." "On 1993-03-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4340m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: CONT DISPLACING WELL TO 1,15 SG NACL BRINE. FINAL NTU READING 52 NTU. PERFORMED TORQUE READINGS AFTER WELL DISPLACED TO BRINE." "On 1993-03-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4340m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESS TESTED TIE-BACK PACKER/CASING TO 345 BAR/15 MIN" "On 1993-03-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 9.0 hours. Operational details: PUMPED 3 M3 CACL2 BRINE SLUG AND POOH." "On 1993-03-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 6.5 hours. Operational details: RIH TO TEST BOP, TEST PLUG LEAKED. POOH AND CHANGED SEAL, RIH AND ATTEMPTED TO TEST BOP, PLUG LEAKED. POOH AND SET PLUG (SPRING LOADED TOOL) TO RETRIEVE WEAR BUSHING. RIH AND LANDED IN WB WITH 10 MT DOWN- WEIGHT. CLOSED MPR AND PRESS TESTED BOP 35 BAR/345 BAR, ANNULAR BAGS PRESS TESTED 35 BAR/240 BAR" "On 1993-03-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: CONT PRESS TESTING BOP. OPENED MPR AND POOH WITH TEST PLUG. CLOSED SHEAR RAM WITH ACCOUSTIC FROM BRIDGE, NO INDICATION ON PANEL, CHECKED FLUID COUNTER IN KOOMEY UNIT, INDICATED CLOSED RAM." "On 1993-03-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.0 hours. Operational details: CLEANED MUD PITS AND ALL LINES TO PREPARE FOR COMPLETION FLUID. CLEANED DERRICK AND RIG FLOOR. PRESS TESTED K/C MANIFOLD WHILE CLEANING RIG." "On 1993-03-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 18.0 hours. Operational details: CONTINUED CLEANING UNDERNEATH RIGFLOOR, PITS AND ALL LINES TO PREPARE FOR COMPLETION FLUID. OPENED UP PLUGGED DRAINS. WHILE CLEANING PRESS TESTED RIG CHOKE MANIFOLD, STAND PIPE TO 35 BAR 5 MIN AND 345 BAR/10 MIN." "On 1993-03-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.5 hours. Operational details: CONTINUED CLEANING RIG FLOOR AND PITS." "On 1993-03-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: M/U DUMMY FLUTED HANGER TO X-OVERS, L/D ON DECK. M/U SSTT TO X-OVERS AND PUP JOINTS." "On 1993-03-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: CONTINUED M/U SSTT AND LUBRICATOR VALVE TO X-OVERS/PUP JOINTS" "On 1993-03-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: CLEANED RIG FLOOR. HELD MEETING ON RIG FLOOR WITH PERSONEL INVOLVED IN BHA RUNNING OPERATION. PREPARED TO RUN TCP GUNS." "On 1993-03-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 425m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 13.0 hours. Operational details: PREPARE TO RUN TCP GUNS. RIH WITH TCP ASSEMBLIES AND LPR-N VALVE, PRESS TESTED STRING TO 200 BAR/15 MIN, CONT RIH WITH TEST STRING BHA AND ONE 4 1/2' PH6 TUBING JNT. PRESS TESTED BHA TO 345 BAR/15 MIN." "On 1993-03-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 550m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CONT RIH WITH 4 1/2' PH6 TUBING TO 550 M. FILLED STRING COMPLETLY WITH 1,15 SG BRINE EVERY 10 SINGLES" "On 1993-03-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1401m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 6.0 hours. Operational details: CONT RIH WITH TEST TUBING FROM 550 TO 1401 M" "On 1993-03-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3055m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 9.0 hours. Operational details: CONT RIH WITH 4 1/2' PH-6 TEST TUBING FROM 1501 TO 3055 M. FILLED STRING WITH 1,15 SG BRINE" "On 1993-03-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3055m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: P/U FLOWHEAD AND M/U TO ONE SINGLE 4 1/2' PH-4 TUBING, L/D SAME" "On 1993-03-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3097m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CONT RIH WITH 4 1/2' PH4 TEST TUBING FROM 3055 TO 3097 M" "On 1993-03-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3097m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: INSTALLED X-OVER ON TEST STANDPIPE" "On 1993-03-30, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3751m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.5 hours. Operational details: CONT RIH WITH 4 1/2' PH-4 TEST TUBING FROM 3097 TO 3751 M" "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4231m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: CONT RIH WITH TEST TUBING FROM 3097 TO 4231 M" "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4231m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: M/U X-OVER ON TEST TUBING, PRESS TEST TEST TUBING TO 350 BAR/10 MIN" "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4312m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: M/U BACK-UP FLUTED HANGER AND RIH WITH TEST STRING ON 5' DP." "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: CONT RIH WITH TEST TUBING AND BACK-UP FLUTED HANGER, LANDED HANGER IN WELLHEAD" "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: R/U ATLAS WIRELINE EQUIP FOR RUNNING GR/CCL LOGS" "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: RIG WITH GR/CCL LOGS TO 2000 M, POOH TO CHANGE TOOL OD FROM 2 1/8' TO 1 11/16'" "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: RIH WITH GR/CCL LOGS FOR TUBING CORRELATION, CORRELATED AGAINST RADIOACTIVE MARKER IN LINER, POOH WITH LOGGING TOOLS. R/D AWS WIRELINE EQUIPMENT" "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CLOSED MPR 0N SSTT SLICK JOINT TO CHECK SPACEOUT, POOH WITH BACK-UP FLUTED HANGER. L/D DP LANDING STRING." "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: P/U SSTT/LUB VALVE CONTROL PANEL/HOSE REEL. P/U GLYCOL INJECTION UNIT." "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: SPACED OUT STRING WITH PUP JOINTS , M/U SSTT TO TEST STRING. H/U CONTROL HOSES AND FUNCTION TESTED SSTT. RIH WITH SSTT ON LANDING STRING, M/U LUBRICATOR VALVE TO TEST STRING, H/U CONTROL LINES AND FUNCTION TESTED." "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4324m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESS TESTED DOWN TEST TUBING AGAINST LPR-N VALVE TO 350 BAR - NEG." "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4324m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: PRESS TESTED SURFACE EQUIPMENT 350 BAR." "On 1993-03-31, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4310m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: PULLED LUBRICATOR VALVE ABOVE ROTARY. PRESS TESTED TEST STRING 350 BAR PRESS DROPPED 5 BAR IN 17 MIN. BLEED OFF PRESSURE TO 250 BAR, PRESS DROPPED 20 BAR IN 1 HR." "On 1993-04-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4310m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: L/D FLOWHEAD WITH COFLEXIP HOSE ON DECK. CHANGED OUT BAILS. L/D LUBRICATOR VALVE AND POOH WITH 3 STANDS TUBING" "On 1993-04-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4220m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: PULLED SSTT ABOVE ROTARY AND PRESS TESTED STRING AGAINST LPR VALVE TO 350 BAR, PRESS DROPPED 8 BAR IN 17 MIN" "On 1993-04-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: L/D SSTT AND PUP JOINTS. PRESS TESTED TUBING 350 BAR" "On 1993-04-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: PRESS TESTED TUBING AGAINST LPR-N VALVE TO 350 BAR/15 MIN" "On 1993-04-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4220m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: SERVICE BROKE SSTT AND L/D SAME. P/U BACK-UP SSTT AND M/U TO TEST STRING. H/U CONTROL LINES AND FUNCTION TESTED SSTT. PRESS TESTED STRING AGAINST LPR-N TO 350 BAR/20 MIN." "On 1993-04-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4260m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: RIH WITH LANDING STRING TO 4260 M, LOST PRESS ON SSTT CONTROL LINE. POOH AND FOUND LEAK ON SSTT, L/D SAME." "On 1993-04-01, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'interruption -- repair' and lasted for 12.0 hours. Operational details: HRS WORKED ON REPAIRING LEAKING SSTT`S RECEIVED NEW SSTT WITH HELICOPTER, PRESS TESTED SAME ON DECK PRIOR TO P/U ON DRILL FLOOR" "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'interruption -- repair' and lasted for 5.0 hours. Operational details: PRESS TESTED NEW SSTT BODY AND BELOW BALL/FLAPPER 350 BAR/10 MIN HAD PROBLEMS WITH LEAKING HOSES AND NEEDLE VALVES." "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: R/U NEW SSTT AND CONTROL MANIFOLD. M/U CONNECTIONS AND PUP JNTS/X-OVER ON SSTT, H/U CONTROL LINES AND FUNCTION TESTED TREE." "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: CONT FUNCTION TESTED NEW SSTT. REPLACED SSTT CONTROL MANIFOLD DUE TO PROBLEMS WITH HYDRAULIC PUMPS." "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: PRESS TESTED SSTT/TUBING - NEG, VOL INCREASED AT TRIP TANK. PULLED SSTT ABOVE ROTARY TO CHECK FOR LEAKS, PRESS TESTED SSTT/TUBING - NEG, NO LEAK OBSERVED AT SURFACE, OBSERVED VOLUME INCREASED IN TRIP TANK L/D SSTT ON DECK" "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESS TESTED TUBING - NEG, OBSERVED VOL INCREASE ON TRIP TANK" "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4200m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: L/D LUBRICATOR VALVE/SSTT FLUTED HANGER. R/D SSTT HOSE REEL AND PUMPING MANIFOLD" "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 430m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 9.5 hours. Operational details: POOH WITH 4 1/2' TEST STRING DUE TO LEAK, RACKED BACK IN DERRICK" "On 1993-04-02, at Well NO 15/9-19 S, a drilling event occurred at a depth of 210m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: POOH WITH BHA, FOUND LEAK IN HRS RD SAFETY CIRC VALVE." "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 5.0 hours. Operational details: CONT POOH WITH BHA AND PERFORATION GUNS" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: BROKE OFF X-OVERS AND PUP JOINTS FROM HRS SSTT AND LUBRICATOR VALVE" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: CONT SERVICE BREAK LUBRICATOR VALVE AND SSTT WITH FLUTED HANGER" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: PREPARED BSC PERFORATION GUNS TO BE RUN IN HOLE" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 217m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: RIH WITH PERF GUNS AND LPR-N ASSY" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 217m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 3.5 hours. Operational details: PRESS TESTED BHA BELOW LPR-N VALVE AGAINST BLIND PLUG TO 200 BAR - NEG FOUND LEAK ON X-OVER ABOVE BLANKING PLUG, REPAIRED SAME. PRESS TESTED AGAINST BLIND PLUG 200 BAR/15 MIN" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 448m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: RIH WITH BHA, FILLED BHA ABOVE LPR-N VALVE WITH 250 LTR VISC PILL" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 448m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: PRESS TESTED BHA AGAINST LPR-N VALVE 350 BAR" "On 1993-04-03, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1044m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: RIH WITH 4 1/2' TEST TUBING TO 1044 M" "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2972m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 6.0 hours. Operational details: CONT RIH WITH TEST TUBING FROM 1044 TO 2972 M FILLED STRING WITH 1,15 SG BRINE" "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2972m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESS TESTED TUBING 350 BAR/15 MIN" "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3030m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: RIH WITH 1 STD 4 1/2' PH-4 TUBING. P/U FLOWHEAD AND M/U ONE SINGLE TUBING BELOW, L/D SAME" "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3227m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.0 hours. Operational details: CONT RIH WITH 4 1/2' PH-4 TEST TUBING TO 3199 M RTTS PACKER DEPTH. TOOK 20 MT WEIGHT, WORKED STRING FREE. RIH, TOOK 10 MT WEIGHT AT 3208 AND 3216 M. WORKED STRING OUT, NOT ABLE TO PASS 3205 M, ATTEMPTED TO PULL STRING FREE WITH MAX 40 MT O/P, WORKED STRING DOWN AND CAME FREE WITH 25 MT D/W. RESIPROCATED STRING BETWEEN 3205 AND 3227 M." "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4230m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: CONT RIH WITH TUBING TO 4230 M" "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4230m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESS TESTED TUBING TO 350 BAR/15 MIN" "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4230m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: SPACED OUT STRING, P/U EZ-TREE WITH FLUTED HANGER AND M/U TO TUBING" "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4230m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.0 hours. Operational details: R/U EZ-TREE CONTROL MANIFOLDS AND HOSE REEL. FUNCTION TESTED EZ-TREE. PRESS TESTED TUBING/EZ-TREE 350 BAR, BLEED OFF PRESS TO 250 BAR AND TESTED EZ-TREE FROM BELOW." "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: RIH WITH TUBING LANDING STRING, P/U LUBRICATOR VALVE AND M/U TO STRING CHANGED TO LONG BAILS AND R/U ATLAS SHEEVE IN TDS. M/U ONE SINGLE TUBING AND LANDED TUBING STRING IN WELLHEAD." "On 1993-04-04, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: R/U ATLAS WIRELINE GR/CCL LOGGING TOOLS AND RIH FOR TUBING CORRELATION" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: CONT CORRELATION TUBING WITH GR/CCL LOG. POOH AND R/D ATLAS WIRELINE EQUIPMENT" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.5 hours. Operational details: PRESS TESTED TUBING/LUB VALVE TO 350 BAR, BLEED OFF PRESS TO 250 BAR, CLOSED LUBRICATOR VALVE AND TESTED FROM BELOW. PRESS TESTED LUBRICATOR VALVE FROM ABOVE TO 350 BAR" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: POOH AND L/D ONE SINGLE TUBING. P/U FLOWHEAD AND M/U TO TUBING. R/U COFLEXIP HOSES AND CONTROL EQUIPMENT" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: M/U FLOWHEAD KILL AND PRODUCTION COFLEXIP HOSES. R/U SURFACE CONTROL EQUIPMENT" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 4.0 hours. Operational details: PRESS TESTED KILL LINE AGAINST FLOWHEAD KILL VALVE 350 BAR. PRESS TEST FLOWHEAD AGAINST CLOSED LUBRICATOR VALVE 350 BAR, CLOSED AND PRESS TESTED MASTER VALVE WITH 350 BAR BELOW AND 35 BAR ABOVE. FLUSHED LINES TO BURNERS AND PRESS TESTED 350 BAR AGAINST CHOKE MANIFOLD. PRESS TEST KILL VALVE FROM WELL SIDE TO 350 BAR." "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 5.0 hours. Operational details: ATTEMPTED TO SET RTTS PACKER SEVERAL TIMES, NO WEIGHT INDICATION OF PACKER SETTING" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESS UP ANNULUS TO 110 BAR, LPR-N OPENED AT 50 BAR. HAD FULL COMMUNICATION BETWEEN ANNULUS AND TUBING." "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: PULLED OUT 8 M AND ATTEMPTED TO SET RTTS PACKER - NEG." "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4338m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: R/D COFLEXIP HOSES AND L/D FLOWHEAD. CHANGED BAILS AND L/D LUBRICATOR VALVE" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4230m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: POOH WITH LANDING STRING. L/D EZ-TREE AND PUP JOINTS. R/D EZ-TREE CONTROL EQUIP AND CLEANED RIG FLOOR" "On 1993-04-05, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4170m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: POOH WITH 4 1/2' TEST TUBING DUE TO PROBLEMS SETTING RTTS PACKER. PULLED SLOW DUE TO PROBLEMS WITH STRING HANGING UP FROM 4230 M. WORKED PIPE FREE." "On 1993-04-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3100m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 6.0 hours. Operational details: CONT POOH WITH TEST TUBING, HAD PROBLEMS WITH STRING HANGING UP FROM 4170 TO 3900 M, WORKED PIPE UP AND DOWN SEVERAL TIMES TO FREE PIPE. MAX OVERPULL 25 MT, NO INDICATION OF STRING TAKING DOWNWEIGHT." "On 1993-04-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 448m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 6.0 hours. Operational details: CONT POOH WITH 4 1/2' TEST TUBING FROM 3100 TO 448 M." "On 1993-04-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 7.5 hours. Operational details: POOH WITH BHA, L/D HRS TOOLS AND TCP GUNS. FOUND 6 EA SLIPS, 3 EA LOCKING SEGMENTS AND 3 EA BOLTS MISSING FROM HRS RTTS RETRIVEABLE PACKER. FUL-FLO BYPASS VALVE WAS BELLED OUT AND CRACKED." "On 1993-04-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: WAITED ON ATLAS WIRELINE TO ARRIVE ONBOARD WITH HELICOPTER. WHILE WAITING SERVICED TDS AND CLEANED RIG FLOOR." "On 1993-04-06, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: R/U ATLAS WIRELINE EQUIPMENT, PREPARED TOOLS FOR RUNNING MAGNET." "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: RIH WITH 6,75' ELECTRO-MAGNET FISHING TOOL ON ATLAS WIRELINE RUN Æ1 TO TOP LINER PBR AT 3191 M, SLACKED OFF 3 M CABLE. ACTIVATED MAGNET 30 M ABOVE LINER PBR POOH WITH MAGNET, RECOVERED 1 EA SEGMENT, 1 EA SLIPS FROM RTTS PACKER, AND 1 EA CUP IRON JUNK." "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 300m. The activity was categorized as 'interruption -- fish' and lasted for 2.5 hours. Operational details: RIH WITH 6,75' ELECTRO-MAGNET FISHING TOOL WITH ATLAS WIRELINE RUN Æ2 TO 3191, SLACKED OFF 3M CABLE AND POOH TO 300 M." "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 0.5 hours. Operational details: CONT POOH WITH 6,75' ELECTRO-MAGNET FISHING TOOL ON ATLAS WIRELINE RUN Æ2, RECOVERED 1 EA BOLT AND HALF CUP IRON JUNK." "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- fish' and lasted for 3.5 hours. Operational details: RIH WITH ELECTRO-MAGNET ON ATLAS WIRELINE RUN Æ3 TO 2191 M, POOH RECOVERED 1/2 CUP IRON JUNK. R/D ATLAS WIRELINE EQUIP" "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: PREPARED TO RUN MILL FOR LINER PBR ASSY, P/U BHA ASSY." "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3160m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 8.0 hours. Operational details: RIH WITH 4 1/2' TUBING AND 5' DRILLPIPE TO 3160 M" "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3191m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: WASHED DOWN FROM 3160 TO TOP LINER TIE-BACK PACKER PBR AT 3191, CLEANED TOP PBR, ENTERED PBR 1 M AND PULLED OUT ABOVE PBR, REPEATED OPERATION IN 1 M STEPS DOWN TO 3197 M, TOOK WEIGHT AND POLISHED TOP PBR. ROTATED PIPE 30 RPM AND PUMPED WITH 1600 L/MIN DURING WHOLE OPERATION." "On 1993-04-07, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1377m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: POOH WITH TUBING/DP TO 1377 M" "On 1993-04-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.0 hours. Operational details: CONT POOH WITH PBR MILL FROM 1377 M" "On 1993-04-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: P/U AND BREAK OFF ONE SINGLE TUBING BELOW HRS FLOWHEAD, L/D SAME" "On 1993-04-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 154m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: M/U BHA WITH 6' MILL AND RIH TO 154 M" "On 1993-04-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2200m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 5.5 hours. Operational details: CONT RIH WITH 6' MILL FROM 154 TO 2200 M" "On 1993-04-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2200m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: CUT AND SLIPPED DRILL LINE" "On 1993-04-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4500m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.0 hours. Operational details: CONT RIH FROM 2200 TO 4500 M WASHED LINER PBR/HANGER AREA FROM 3188 TO 3205 M" "On 1993-04-08, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 7.5 hours. Operational details: POOH WITH 6' MILL" "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.0 hours. Operational details: M/U BOP TEST TOOL AND RIH. PRESS TESTED BOP - NEG. POOH WITH TEST TOOL CHANGED SEAL ON TEST TOOL, M/U JET TOOL AND RIH WITH JET TOOL SUB AND BOP TEST TOOL. WASHED WELLHEAD AND LANDED TEST TOOL IN WELLHEAD." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.5 hours. Operational details: PRESS TESTED BOP AGAINST TEST PLUG 345 BAR, DROPPED 5 BAR/5 MIN, BRINE LEAKING OUT OF DP. BLEED OFF PRESS AND PULLED TEST TOOL ABOVE BOP, GAINED 1 M3 BRINE ON TRIP TANK. FLOWCHECKED - WELL STABLE." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: LANDED TEST TOOL IN WELLHEAD AND PRESS TESTED BOP MPR 345 BAR" "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: CONTINUED PRESSURE TESTING BOP." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.5 hours. Operational details: KILL HOSE BURSTED. CONTINUED BOP-TESTING DOWN CHOKE LINE. TESTED ACOUSTIC SYSTEM AND FUNCTION TESTED BOP ON BLUE POD." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: INSTALLED NEW KILL HOSE. PRESSURE TESTED SAME TO 345 BAR/15 MINS." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: CLOSED UAP. LIFTED TEST TOOL FROM WELLHEAD AND OBSERVED FOR ANY PRESSURE BUILD-UP, NEGATIVE." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: OPENED UAP. OBSERVED WELL FLOWING, GAINED 1,1 M3. CIRCULATED BOTTOMS UP, MAX GAS 0,49%. POOH WITH SPRING LOADED TOOL." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: RIH TO RETRIEVE WEAR BUSHING. ENGAGED WEAR BUSHING. POOH, LEFT WEAR BUSHING IN WELLHEAD. REPEATED ATTEMPT TO RETRIEVE WEAR BUSHING, NEGATIVE." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: MADE UP JET TOOL. RIH AND WASHED WELLHEAD. POOH. RIH WITH SPRING LOADED TOOL AND RETRIEVED WEAR BUSHING. POOH." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: FLUSHED SURFACE LINES. ATTEMPTED TESTING SHEAR RAM AGAINST CASING/SEAL ASSEMBLY, NEGATIVE. TESTED SURFACE LINES AGAINST FAIL SAFE TO 345 BAR OK. OPERATED SHEAR RAM, CHANGED TO YELLOW POD AND ATTEMPTED TESTING SHEAR RAM, NEGATIVE. SHEAR RAM LEAKING. PUMPED VOLUME IN RETURN TO TRIP TANK." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: RIH WITH JET TOOL. WASHED SHEAR RAM AREA. CLOSED UPR AND PRESSURE TESTED CASING/SEAL ASSEMBLY AGAINST UPR TO 345 BAR/30 MINS, OK." "On 1993-04-09, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: POOH. CLOSED SHEAR RAM. ATTEMPTED PRESSURE TESTING SHEAR RAM, NEG." "On 1993-04-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: DISPLACED RISER TO SEA WATER. OBSERVED WELL, WELL STATIC." "On 1993-04-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 5.5 hours. Operational details: PREPARED TO PULL BOP." "On 1993-04-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: P/U LANDING JOINT AND CONTINUED PREPARATIONS TO PULL BOP. DISCONNECTED AT 08:45 HRS. DE-BALLASTED RIG 3M." "On 1993-04-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.0 hours. Operational details: MOVED RIG 25M STARBOARD" "On 1993-04-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 4.5 hours. Operational details: DISCONNECTED KILL- AND CHOKE HOSES AND RUCKER LINES. PULLED BOP TO 33M." "On 1993-04-10, at Well NO 15/9-19 S, a drilling event occurred at a depth of 33m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: WAITED ON WEATHER TO PULL BOP THROUGH SPLASH ZONE." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 33m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: CONT. W.O.W." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 29m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: PULLED BOP TO 29M, L/D RISER PUP JOINT." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 29m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: CONT. W.O.W." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 29m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: CONT. W.O.W." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: PULLED BOP THROUGH SPLASH ZONE. PREPARED TO LAND BOP ON CARRIER." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: LANDED AND SECURED BOP ON CARRIER." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 12.0 hours. Operational details: OPENED SHEAR RAM DOORS ON BOP AND INSPECTED SEALS. FOUND DAMAGES ON T-SEAL AND ON 1 RAM-TOP SEAL, CHANGED OUT SAME AND CLOSED DOORS." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: PRESSURE TESTED MPR, INNER KILL VALVE AND UPR TO 20/345 BAR, 5/10 MINS ATTEMPTED PRESSURE TESTING SHEAR RAM, NEGATIVE. MAJOR LEAK ACROSS THE RAMS." "On 1993-04-11, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: DRAINED BOP. INVESTIGATED LEAK." "On 1993-04-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 6.0 hours. Operational details: CONT. INVESTIGATING LEAK. OPENED RAM DOORS TO CHECK SEALS. CHECKED RAM OPERATION. FOUND O-RINGS EXTRUDED OUT OF UPPER SEAL SEAT. PREPARED TO REMOVE UPPER SEAL SEAT TO CHANGE OUT O-RINGS." "On 1993-04-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 9.5 hours. Operational details: REMOVED SHEAR RAM UPPER SEAL SEAT. CHANGED OUT O-RINGS AND BACK-UP RING, RE-INSTALLED SEAL SEAT. CLOSED RAM DOORS." "On 1993-04-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: PREPARED TO TEST STACK. ATTEMPTED PRESSURE TESTING SHEAR RAM TWICE, NEGATIVE. PRESSURE TESTED SHEAR RAM OK ON THIRD ATTEMPT TO 20/345 BAR, 5/10 MINS." "On 1993-04-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: FILLED STACK. INSTALLED TEST TOOL. ATTEMPTED PRESSURE TESTING LAP TO 20/345 BAR, NEGATIVE, LEAKED 1 BAR/MIN ON HP-TEST. FUNCTIONED LAP TWICE. SPM-VALVE FAILED." "On 1993-04-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: CHANGED OUT 2 EA SPM VALVES FOR LAP, ON YELLOW POD." "On 1993-04-12, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: OPERATED LAP SEVERAL TIMES. ATTEMPTED PRESSURE TESTING, NEGATIVE." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: ATTEMPTED PULLING TEST TOOL TO INSPECT LAP, NEGATIVE. TOOL HANGING UP. DRAINED STACK. FOUND TEST TOOL HANGING UP IN RUBBER LIP FROM LAP ELEMENT. CUT LOOSE AND REMOVED RUBBER LIP." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: PRESSURE TESTED LAP TO 20/345 BAR, 5/10 MINS. ATTEMPTED PRESSURE TESTING UAP, NEGATIVE ON LOW PRESSURE. OPERATED UAP 3 TIMES. PRESSURE TESTED UAP TO 20/240 BAR, 5/10 MINS. PRESSURE TESTED REMAINING FAIL SAFE VALVES AND SHEAR RAM TO 20/345 BAR, 5/10 MINS." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: CHANGED OUT LEAKING SPM-VALVE, UAP CLOSING FUNCTION ON YELLOW POD. PREPARED BOP FOR RUNNING. MOVED BOP CARRIER IN PLACE." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 7.0 hours. Operational details: M/U 2 EA 50 FT RISER JOINTS TO BOP. INSTALLED GUIDE LINES. BURNT OFF SEA FASTENING. RAN BOP. PRESSURE TESTED K/C-LINES TO 345 BAR WHILE RUNNING BOP. INSTALLED K/C-HOSES, RISER TENSIONERS AND POD HOSE SADLES. DE-BALLASTED RIG 3M." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: MOVED RIG BACK OVER WELL AND RE-BALLASTED RIG." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 104m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: POSITIONED RIG. LANDED BOP, PULL TESTED WITH 25 TONS OVERPULL. STROKED OUT SLIP JOINT. L/D HANDLING JOINT. INSTALLED DIVERTER. CLOSED SHEAR RAM WITH ACOUSTIC. PRESSURE TESTED WELLHEAD CONNECTOR DOWN K/C-LINES AGAINST SHEAR RAM TO 20/345 BAR, 5/10 MINS. FUNCTION TESTED BOP ON YELLOW POD." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: R/D RISER HANDLING EQUIPMENT. R/U PIPE HANDLING EQUIPMENT." "On 1993-04-13, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: SPACED OUT AND MADE UP SPRING LOADED TOOL AND RIH TO RETRIEVE SEAL ASSEMBLY. LANDED OFF IN WELLHEAD. CLOSED LAP AND ESTABLISHED CIRCULATION DOWN KILL, UP CHOKE LINE. PULLED BACK TO RETRIEVE SEAL ASSEMBLY, NO PRESSURE BUILD-UP. POOH, MISRUN." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: CHECKED SPRING LOADED TOOL. RE-RUN TO PULL SEAL ASSEMBLY. LANDED OFF, CLOSED LAP. PULLED BACK 3M. OBSERVED PRESSURE BUILD-UP TO 11 BAR/30 MINS. OBSERVED GAS IN RISER. INCREASED CLOSING PRESSURE ON LAP." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 102m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CIRCULATED THROUGH BOP AT 350 LPM HOLDING 10 BAR BACK PRESSURE." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 102m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: BLED OFF PRESSURE. CLOSED IN TO OBSERVE BUILD-UP: 7 BAR/30 MINS. BLED OFF FROM 7 BAR. PRESSURE BUILT UP TO 5 BAR/20 MINS." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 102m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: CIRCULATED THROUGH BOP AT 350 LPM. BLED OFF PRESSURE. OBSERVED PRESSURE BUILD-UP 1,5 BAR. BLED OFF PRESSURE." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 102m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RELEASED TRAPPED GAS FROM BOP AND DRILL STRING. OPENED LAP. FLOW CHECKED 15 MINS, NEG. POOH WITH SEAL ASSEMBLY TO 30M." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: CONTINUED POOH AND L/D SEAL ASSEMBLY." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: RIH WITH CEMENT CLEAN-OUT TOOL. WASHED WELLHEAD. POOH." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: RIH WITH METAL-TO-METAL SEAL ASSEMBLY. INSTALLED AND PRESSURE TESTED SAME TO 345 BAR/10 MINS." "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 105m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: INSTALLED WEAR BUSHING" "On 1993-04-14, at Well NO 15/9-19 S, a drilling event occurred at a depth of 404m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 13.5 hours. Operational details: CLEANED RIG FLOOR AND PREPARED FOR RUNNING DST-STRING. RIH WITH DST-BHA. PRESSURE TESTED RTTS-PACKER, LPR-N, BUNDLE CARRIER AND FULL-FLO BYPASS VALVE TO 200 BAR/10 MINS. SERVICE BROKE AND CHECKED EACH CONNECTION ON 4 3/4' DC." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 443m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: CONT. RIH WITH DST-STRING. CONTINUED RUNNING/SERVICE BROKE 4 3/4' DRILL COLLARS. M/U 2 EA TUBING JOINTS." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 443m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESSURE TESTED SURFACE LINES TO 20/345 BAR. ATTEMPTED PRESSURE TESTING DST-STRING AGAINST LPR-N. 20 BAR OK. 345 BAR, NEGATIVE, PRESSURE DROPPED 0,5 BAR/SEC." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 397m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: L/D 2 EA TUBING JOINTS. ATTEMPTED PRESSURE TESTING DST-STRING, NEG. PULLED BACK 4 EA SLIP JOINTS. ATT. PRESSURE TESTING DST-STRING, NEG. L/D SLIP JOINTS. PULLED AND RACKED BACK 2 STANDS DRILL COLLARS. PRESSURE TESTED OK. RAN BACK IN WITH 1 STAND DRILL COLLAR, PRESSURE TESTED OK. RAN BACK IN WITH LAST STAND DRILL COLLAR, TESTED OK 345BAR" "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: P/U SLIP JOINTS AND 1 SINGLE PH-6 TUBING. PRESSURE TESTED DST STRING AGAINST LPR-N VALVE TO 345 BAR/10 MINS." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1684m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 4.5 hours. Operational details: CONT. RIH WITH DST STRING TO 1684M. FILLED STRING EACH 5 JOINTS." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1684m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: PRESSURE TESTED DST STRING AGAINST LPR-N VALVE TO 345 BAR/10 MINS." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2680m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.5 hours. Operational details: CONT. RIH TO 2680M." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2987m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: WHILE RECIPROCATING STRING, WORKED 2 LEFT HAND TURNS INTO STRING. CONT. RIH TO 2987M." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2987m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESSURE TESTED DST-STRING AGAINST LPR-N VALVE TO 345 BAR/10 MINS." "On 1993-04-15, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 5.0 hours. Operational details: RECIPROCATED STRING AND WORKED 2 TURNS LEFT HAND TORQUE INTO STRING. CONT. RIH." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4237m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: CONT. RIH TO 4237M." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4237m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: PRESSURE TESTED DST STRING AGAINST LPR-N VALVE TO 345 BAR/10 MINS." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: P/U SUBSEA TEST TREE/FLUTED HANGER AND M/U TO DST STRING. CHECKED LATCH FUNCTION. CHECKED GLYCOL INJECTION SYSTEM. VERIFIED VALVE OPERATION." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: PRESSURE TESTED DST STRING AGAINST LPR-N VALVE TO 345 BAR/10 MINS. VERIFIED GLYCOL INJECTION AGAINST 300 BAR INSIDE STRING. VERIFIED CHECK VALVE HOLDING. CLOSED SSTT AND TESTED SAME FROM BELOW TO 225 BAR DIFFERENTIAL PRESSURE/10 MINS." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: P/U LANDING STRING. INSTALLED LUBRICATOR VALVE AND FUNCTION TESTED SAME. CHANGED TO 40 FT BAILS. P/U 1 PUP JOINT AND 1 SINGLE. LANDED STRING IN WELLHEAD. CLEANED RIG FLOOR." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: R/U AWS. RIH WITH GR/CCL TO CORRELATE DEPTH. POOH. R/D AWS." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.5 hours. Operational details: L/D 1 SINGLE. PRESSURE TESTED DST STRING AGAINST LPR-N VALVE TO 345 BAR/10 MINS. PRESSURE TESTED LUBRICATOR VALVE FROM BELOW TO 250 BAR." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.5 hours. Operational details: P/U FLOWHEAD. CONNECTED KILL/PRODUCTION HOSES AND CONTROL HOSES." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: LANDED DST STRING IN WELLHEAD. ATTEMPTED PRESSURE TESTING, NEGATIVE. OBSERVED LEAK IN CEMENT UNIT." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: CHANGED ALL 3 DISCHARGE VALVES ON 2 3/4' CEMENT PUMP. FOUND 2 DAMAGED." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.5 hours. Operational details: PRESSURE TESTED LINES/HOSE FROM CEMENT UNIT AGAINST KILL VALVE TO 345 BAR/10 MINS. PRESSURE TESTED SWAB VALVE FROM BELOW TO 345 BAR/10 MINS TESTED MASTER VALVE FROM BELOW TO 345 BAR/10 MINS. FLUSHED THROUGH LINES TO BURNERS. TESTED UPSTREAM VALVES ON CHOKE MANIFOLD TO 345 BAR/ 10 MINS. TESTED KILL VALVE FROM BELOW TO 345 BAR/10 MINS." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: ATTEMPTED TO PICK UP DST STRING TO SPACE OUT FOR PACKER SETTING, NEG. STRING HUNG UP AFTER PULLING 3M (2,2 M ABOVE UPWEIGHT). MAX OVERPULL 15 TONS. REMOVED MASTER BUSHING AND WORKED STRING FREE." "On 1993-04-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: SPACED OUT BY PULLING 3,6 M. SET RTTS BY ROTATING AT MAX. 9000 FTLBS AND SET DOWN WEIGHT. RE-LANDED FLUTED HANGER. SET DOWN 35 TONS ON FLUTED HANGER. CLOSED MPR." "On 1993-04-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: PRESSURE TESTED RTTS FROM ABOVE TO 110 BAR DIFFERENTIAL FROM ABOVE FOR 15 MINS." "On 1993-04-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CYCLED OMNI FROM POS. 3 1/2 TO CIRCULATION POS. 11 1/2." "On 1993-04-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.5 hours. Operational details: LINED UP NBS FOR DIRECT SUCTION OF DIESEL. CIRCULATED 24,4 M3 DIESEL DOWN DST STRING AT 500 LPM. DISPLACED DIESEL WITH 0,5 M3 MEG." "On 1993-04-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CYCLED OMNI VALVE TO WELL TEST POSITION 2." "On 1993-04-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: HELD PRE-OPERATION MEETINGS WITH INVOLVED PERSONELL. INSPECTED RIG FLOOR AND WELL TEST AREAS. CHECKED ALL LINES AND VALVES. TESTED ESD-SYSTEMS." "On 1993-04-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: OPENED KILL VALVE. PRESSURED UP DST STRING TO 330 BAR AGAINST CLOSED CHOKE TO FIRE GUNS. CLOSED KILL VALVE. BLED DOWN STRING PRESSURE. PERFORATED WELL FROM 4338,0M TO 4316,0M MD AT 05:57 HRS. STARTED FLOW TO TANK." "On 1993-04-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 18.0 hours. Operational details: FLOWED WELL FOR CLEAN-UP. SHUT-IN WELL FOR BUILD-UP BY CLOSING LPR-N VALVE AT 23:57 HRS. CLOSED CHOKE AT 23:59 HRS." "On 1993-04-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.0 hours. Operational details: WELL SHUT-IN FOR BUILD-UP." "On 1993-04-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 12.5 hours. Operational details: WELL SHUT-IN FOR BUILD-UP." "On 1993-04-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: OPENED WELL AT LPR-N VALVE (18:22 HOURS) AND CHOKE MANIFOLD FLOWED WELL ON 23/64' ADJUSTABLE CHOKE PRIOR TO RUN WIRELINE. SHUT IN WELL ON CHOKE MANIFOLD AT 19:10 HOURS." "On 1993-04-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: CLOSED LUB. VALVE AND CHECKED THAT SAME HELD PRESSURE FROM BELOW. INSTALLED SPS TOOLSTRING AND PRESSURE TESTED W.L. LUBRICATOR/STUFFING- BOX TO 250 BAR AGAINST LUB.VALVE AND FAILSAFE VALVE.EQUILIZED PRESSURE ACROSS LUB. VALVE AND OPENED SAME." "On 1993-04-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4316m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: RIH WITH 1,90' OD BLIND BOX ON SLICK LINE TO 4316M TO VERIFY FREE PASSAGE AND GUNS DROPPED." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4316m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: CONT. WIRELINING: POOH WITH BLIND BOX. CLOSED LUBRICATOR AND INFLOW TESTED SAME." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 2.0 hours. Operational details: R/D BLIND BOX TOOLSTRING. M/U TOOLSTRING WITH 2 EA PETROTECH AND 2 EA SCHLUMBERGER BOTTOMHOLE SAMPLERS AND 1 MEMORY GAUGE AND INSTALLED SAME IN TEST STRING. PRESSURE TESTED LUBRICATOR TO 30/250 BAR, 5/10 MINS." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: EQUALIZED ACROSS LUBRICATOR VALVE AND OPENED SAME. OPENED UP WELL ON 12/64' CHOKE AT 05:12 HRS. RIH WITH BHS WHILE FLOWING WELL ON 12/64' FIXED CHOKE." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3900m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 4.5 hours. Operational details: CONTINUED RIH WITH BHS TO 3900M WHILE FLOWING WELL ON 12/64' CHOKE. HAD PICK-UP WEIGHT 430 KG AT 3900M WHILE FLOWING. SHUT IN WELL AT 10:15 HRS." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: TOOK BOTTOM HOLE SAMPLES." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: FLOWED WELL ON 12/64' CHOKE FROM 11:43 HRS WHILE POOH WITH BHS, SHUT IN WELL AT 12:11 HRS. TOOK GRADIENT STOPS AT 3870M, 3840M AND IN LUBRICATOR WHILE POOH." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: CLOSED LUBRICATOR AT 13:34 HRS. VERIFIED LUBRICATOR VALVE HOLDING PRESSURE FROM BELOW." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.0 hours. Operational details: RIGGED DOWN BHS AND WIRELINE EQUIPMENT. TESTED SWAB VALVE AGAINST PROD.WING / LUBRICATOR VALVE TO 250 BAR. MADE SEVERAL ATTEMPTS TO PRESSURE TEST LUBRICATOR VALVE FROM BELOW BY BLEEDING DOWN TO 35 BAR ABOVE, NEG. OBSERVED VALVE LEAKING. EQUALIZED ACROSS LUBRICATOR VALVE AND OPENED SAME." "On 1993-04-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 5.0 hours. Operational details: OPENED WELL FOR MAIN FLOW PERIOD AT 19:24 HRS." "On 1993-04-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.0 hours. Operational details: CONTINUED MAIN FLOW." "On 1993-04-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 18.0 hours. Operational details: CONTINUED MAIN FLOW PERIOD." "On 1993-04-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.5 hours. Operational details: CONTINUED MAIN FLOW PERIOD." "On 1993-04-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 4.5 hours. Operational details: CLOSED IN WELL ON LPR-N VALVE AT 01:42 HRS. VERIFIED LPR-N VALVE CLOSED BY BLEEDING DOWN TUBING PRESSURE 20 BAR. CLOSED CHOKE MANIFOLD. WELL SHUT-IN FOR BUILD-UP." "On 1993-04-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 18.0 hours. Operational details: WELL SHUT-IN AT LPR-N VVALVE AND CHOKE MANIFOLD FOR BUILD-UP." "On 1993-04-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.0 hours. Operational details: WELL SHUT-IN AT LPR-N VVALVE AND CHOKE MANIFOLD FOR BUILD-UP." "On 1993-04-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 16.5 hours. Operational details: WELL SHUT INN ON LPR-N AND CHOKE MANIFOLD FOR MAIN BUILD-UP." "On 1993-04-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: BLED OFF GAS FROM TEST TUBING THROUGH CHOKE MANIFOLD TO BURNER UNTIL WHP BELOW 10 BAR." "On 1993-04-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: CLOSED FLOW HEAD WING VALVE AND CHOKE MANIFOLD. OPENED FLOW HEAD KILL VALVE." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: PUMPED 18,6 M3 1,15 SG NACL BRINE DOWN TEST STRING WITH CEMENT UNIT AT 600 LPM TO REFILL STRING, PRESSURED UP TO 110 BAR TO EQUALIZE ACROSS LPR-N VALVE." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 2.0 hours. Operational details: OPENED LPR-N VALVE. BULLHEADED GAS/OIL BACK INTO FORMATION BY PUMPING 19,5 M3 1,15 SG NACL BRINE: FIRST 11 M3 AT MAX 90 BAR/1000 LPM, THEN PRESSURE INCREASED FROM 90 BAR TO 290 BAR/815 LPM WHILE PUMPING THE LAST 8,5 M3. TOTAL PUMPED 38,1 M3 BRINE. KILLED WELL BY PUMPING 4,0 M3 HI-VIS 1,38 SG MUD AT 630 LPM, PRESSURE INCR. FROM 150 TO 176 BAR," "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.0 hours. Operational details: FOLLOWED BY 27,2 M3 1,38 SG MUD AT TYPICAL 650 LPM/180-200 BAR. MUD HIT PERFORATIONS AFTER HAVING PUMPED 26,7 M3. SLOWED DOWN TO 400 LPM THE LAST 4 M3. PUMPING PRESSURE INCREASED FROM 190 TO 240 BAR THE LAST 0,5 M3. BLED OFF PRESSURE ON CEMENT UNIT." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: FLOW CHECKED WELL 30 MINS." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CLOSED LPR-N VALVE AND LUBRICATOR VALVE. OPENED FLOW HEAD WING VALVE AND CHOKE MANIFOLD. FLUSHED SURFACE LINES TO BURNER ON STARBOARD SIDE. CLOSED FLOW HEAD WING VALVE. OPENED LUBRICATOR VALVE." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: CYCLED OMNI FROM WELL TEST POSITION TO CIRCULATING POSITION 11 1/2. RECORDED 47 BAR U-TUBE PRESSURE." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.5 hours. Operational details: DISPLACED ANNULUS TO 1,38 SG MUD BY CIRCULATING THROUGH OMNI VALVE AND HOLDING BACK PRESSURE ON CHOKE DUE TO U-TUBING. MAX RATE 1000 LPM." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 6.5 hours. Operational details: CONTINUED DISPLACING ANNULUS TO 1,38 S.G. MUD BY CIRCULATING THROUGH OMNI VALVE. CIRCULATED UNTIL GAS READINGS WERE LESS THAN 1%. MAX GAS 6%, MAX RATE 1000 LPM." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: DISPLACED RISER TO 1,38 S.G. MUD THROUGH KILL LINE." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: OPENED MPR AND OBSERVED WELL FOR 10 MIN." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 0.5 hours. Operational details: CIRCULATED WELL, REGISTERED NO GAS. OBSERVED WELL FOR 10 MIN." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4312m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.0 hours. Operational details: RELEASED RTTS PACKER AND FLOWCKECKED 30 MIN." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4312m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 3.5 hours. Operational details: CLOSED MPR AND CIRCULATED WELL UNTIL GAS READINGS WERE UNDER 1%. MAX GAS 1,04%." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4312m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 1.5 hours. Operational details: OPENED MPR, FLOWCHECKED 10 MIN. CONTINUED CIRCULATING UP RISER. FLOWCHECKED 30 MIN." "On 1993-04-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4312m. The activity was categorized as 'formation evaluation -- drill stem test' and lasted for 4.0 hours. Operational details: PUMPED SLUG. RIGGED DOWN CO-FLEX HOSES, LAID DOWN FLOW TREE, CHANGED BAILS AND ELEVATORS." "On 1993-04-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4212m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: SERVICE BROKE AND LAID DOWN LUB.VALVE. POOH AND LAID DOWN LANDING STRING." "On 1993-04-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4202m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: SERVICE BROKE AND LAID DOWN EZ-TREE. CLEARED DRILL FLOOR OF TESTING EQUIMENT." "On 1993-04-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3813m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 3.0 hours. Operational details: POOH AND LAID DOWN TESTING STRING." "On 1993-04-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 403m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 18.0 hours. Operational details: POOH AND LAID DOWN TESTING STRING." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 15m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 6.0 hours. Operational details: POOH AND LAID DOWN TESTING STRING. SERVICE BROKE DST TOOLS AND PACKER WHILE POOH." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: FINISHED POOH AND LAID DOWN TESTING STRING." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 0.5 hours. Operational details: CLEARED FLOOR OF BAKER SAND CONTROL EQUIPMENT." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.5 hours. Operational details: PICKED UP AND BROKE OFF TUBING JOINT FROM SURFACE FLOW TREE AND SERVICE BROKE SAME." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'formation evaluation -- rig up/down' and lasted for 1.0 hours. Operational details: CLEARED FLOOR OF REMAINING TESTING EQUIPMENT. REARRANGED COFLEXIP HOSE AND TAPE MEASURED HIGHT IN DERRICK WITH TOPDRIVE IN UPPER MOST POSITION (30 CM FROM CROWN)." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1417m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: RIGGED UP PIPE HANDLING EQUIPMENT, MADE UP BHA AND RAN SAME IN HOLE ON 3 1/2' DRILLPIPE. FILLED PIPE AND BROKE CIRCULATION EVERY 30 STANDS." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1417m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: RIGGED DOWN 3 1/2' DRILL PIPE EQUIPMENT AND RIGGED UP 5' DRILL PIPE EQUIPMENT. REARRANGED SETBACK." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4570m. The activity was categorized as 'plug abandon -- trip' and lasted for 7.0 hours. Operational details: CONTINUED RUNNING IN WITH 5' DRILL PIPE. FILLED PIPE AND BROKE CIRCULATION EVERY 35 STANDS. TAGGED OBSTRUCTION AT 4560M PUSHED SAME DOWN TO BUT COULD NOT PASS 4570M WITH 40 TONN AND CIRCULATION." "On 1993-04-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4570m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.5 hours. Operational details: CIRCULATED AND CONDITIONED MUD UNTIL WEIGTH WAS 1,38 S.G. AROUND. MAX GAS READING 2,39%." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4570m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: PUMPED AND DISPLACED 1,90 S.G. MUD PILL FROM 4570M TO 4333M." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1417m. The activity was categorized as 'plug abandon -- trip' and lasted for 5.5 hours. Operational details: POOH TO 1417M." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: FINISHED POOH AND LAID DOWN MILL AND BIT SUB." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4305m. The activity was categorized as 'plug abandon -- trip' and lasted for 10.0 hours. Operational details: MADE UP EZSV SQUEEZE RETAINER AND RIH WITH SAME TO 4305M." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4305m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 2.5 hours. Operational details: MADE UP KELLY COCK, PUMPIN SUB. SET EZSV PACKER AND LOAD TESTED SAME WITH 17 TONN. PULLED STINGER UP TO 4300M. MADE UP CEMENT HOSE AND TESTED SAME TO 345 BAR, 10 MIN. CLOSED MPR AND TESTED EZSV TO 100 BAR 5 MIN. OPENED MPR." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4305m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.5 hours. Operational details: CLOSED UAP WITH REDUSED OPERATING PRESSURE AND PERFORMED CIRCULATION TEST THROUGH CHOKE. STUNG INTO EZSV AND PUT 20 TONN ON SAME. PERFORMED INJECTION TEST, FORMATION/FILTERCAKE BROKE DOWN AT 300 BAR. INJECTION RATES: 300 BAR - 200 LPM, 320 BAR - 250 LPM, 345 BAR - 275 LPM." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4305m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: VENTLINE ON NBS/BJ SURGETANK PLUGGED UP WITH SEMISOLID CEMENT, UNPLUGGED SAME." "On 1993-04-26, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4303m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 0.5 hours. Operational details: PULLED OUT OF EZSV AND UP TO 4303M. PUMPED 2 M3 FRESH WATER AHEAD OF CEMENT. MIXED AND PUMPED 5 M3 1,90 S.G. SLURRY. KEPT 50 BAR BACKPRESSURE ON ANNULUS TO AVOID U-TUBING." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4303m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 1.0 hours. Operational details: PUMPED 1 M3 FRESH WATER BEHIND CEMENT SLURRY. DISPLACED CEMENT WITH 22,4 M3 1,38 SG MUD. KEPT 50 BAR BACKPRESSURE TO AVOID U-TUBING." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4305m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 0.5 hours. Operational details: STUNG INTO EZSV AND PUT 20 TON ON SAME. PUMPED 0,5M3 FW AND 2,5M3 CMT THROUGH THE EZSV LEAVING 1,9 M3 CMT IN THE WELLBORE BELOW THE EZSV AND SQUEEZING 0,6 M3 CMT INTO THE FORMATION. INIT SQUEEZE RATE 200LPM AT 220BAR. PRESS INCR TO 345BAR AFTER 500LTRS, SHUT DOWN AND OBSERVED BLEED OFF. CONT SQUEEZE W/100LPM AT 286BAR, INCR TO 145LPM AT 275BAR." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4197m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: PULLED STINGER OUT OF EZSV AND BLED OFF U-TUBING THROUGH CHOKE. TOTAL VOLUME BLED BACK WAS 600 LTRS. DISCONNECTED CEMENT HOSE AND POOH TO 4197 M. RECONNECTED CEMENT HOSE." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 4197m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: REVERCED OUT EXCESS CEMENT AND WATER FROM WELL. TOTAL OF CEMENT AND WATER IN RETURNS WAS APPROXIMATLY 4 M3." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2500m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: POOH WITH CEMENT STINGER TO 2500M." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 4.5 hours. Operational details: POOH WITH CEMENT STINGER AND LAID DOWN SAME." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: M/U 9 5/8' EZSV PERMANENT BRIDGE PLUG AND SETTING SLEEVE TO 5' DP." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: PRESSURE TESTED CEMENT PLUG/CEMENT RETAINER AGAINST SHEAR RAM TO 345 BAR/15 MIN." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 400m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: RIH WITH 9 5/8' EZSV BRIDGE PLUG TO 400M." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 400m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: SET EZSV PERMANENT BRIDGE PLUG AND PULLED OFF SETTING SLEEVE WITH 20 TON OVERPULL. LOAD TESTED BRIDGE PLUG WITH 5 TON DOWNWEIGHT." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 400m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: R/U CEMENT HOSE TO PUMPIN SUB AND CIRCULATED TO FLUSH OUT AIR. PRESSURE TESTED SAME TO 345 BAR/5 MIN. CLOSED MPR AND PRESSURE TESTED EZSV BRIDGE PLUG TO 345 BAR/15 MIN. OPENED MPR." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 400m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: PUMPED 2 M3 SEAWATER FOLLOWED BY 9,5 M3 1,90 S.G. CEMENT SLURRY. DISPLACED CEMENT DOWN DP WITH 0,8 M3 SEAWATER." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH WITH 5' DP TO 190 M." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 190m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: REVERSE CIRCULATED OUT EXCESS CEMENT ABOVE 190 M. DUMPED 1,6 M3 GOOD CEMENT AND 1,6 M3 CONTAMINATED MUD/SEAWATER." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: RIGGED DOWN CEMENT HOSE AND POOH W/SETTING SLEEVE AND 5' DP." "On 1993-04-27, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 5.0 hours. Operational details: POOH AND LAID DOWN 60 JOINTS 5' DRILLPIPE AND 66 JOINTS 3 1/2' DRILL PIPE" "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: LAID DOWN 33 JOINTS 3 1/2' DRILL PIPE, 2 JOINTS 5' DRILL PIPE AND TWO DRILLING JARS." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: SLIP AND CUT DRILL LINE." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 188m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: RIH AND TAGGED TOP OF CEMENT WITH 10 TONN AT 188M.DISPLACED WELL TO SEA WATER AND PLACED PACKER FLUID FROM 188M TO WELL HEAD. POOH. PACKER FLUID: FRESH WATER WITH 0,5 KG/M3 BIOSID 0,5 KG/M3 OKSYGEN SCAVENGER PH AT 10 TO 11" "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 60m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: CLOSED SHEAR RAM AND STARTED WASHING RISER." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.5 hours. Operational details: WASHED RISER DOWN TO SHEAR RAM AND TAGGED SAME. OPENED SHEAR RAM, WASHED BOP AND CIRCULATED WELL CLEAN. POOH." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'drilling -- bop activities' and lasted for 8.5 hours. Operational details: RIH WITH SPRING LOADED TOOL AND TESTED BOP TO 35BAR/5MIN, 345BAR/15MIN LAP 20BAR/5MIN, 345BAR/15MIN AND UAP 20BAR/5MIN, 240BAR/15MIN. RETESTED LAP BEFORE GOOD TEST, AND CHANGED LEAKING VALVE ON BJ-UNIT. TESTED ACCOUSTIC FROM BRIDGE." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: LINED UP ON CHOKE MANIFOLD DUE TO SMALL FLOW OVER TOP OF DRILL PIPE DURING BOP TEST (SINCE 12:00 HRS). CLOSED KELLY COCK, OPENED FAIL SAFE VALVES, CLOSED UPR AND RELEASED SPRING LOADED TOOL." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: OBSERVED WELL ON CHOKE MANIFOLD FOR 15 MIN. NO PRESSURE ON CHOKE, NO GAS READINGS IN TRIP TANK." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: OPENED UPR AND RECORDED WELL ON TRIP TANK, GAINED 100 LTRS ON TRIP TANK AND GAS BOILED OUT OF RISER." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: CIRCULATED DOWN CHOKE LINE AND UP RISER AT 1050 LPM. MAX GAS WAS 2.83% FROM BOTTOMS UP (C1=17242,C2=1412,C3=760,IC4=15 AND NC4=169 ALL PPM) CIRCULATED GAS DOWN TO 0,12%. OBSERVED WELL FOR 30 MIN. CONTINUED CIRCULATION DOWN CHOKE UP RISER AT 1050 LPM. MAX GAS AT BOTTOMS UP WAS 0,19% ( ONLY C1=2036 PPM)." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RAN IN AND LATCHED INTO WEAR BUSHING, PULLED WEAR BUSHING FREE WITH 10 TON OVER PULL. POOH, WEAR BUSHING WAS NOT RECOVERED." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RAN BACK IN, LATCHED INTO AND PUT 8 TON ON WEAR BUSHING. PULLED AND RECOVERED WEAR BUSHING." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CIRCULATED DOWN CHOKE LINE AND UP RISER AT 1050 LPM. MAX GAS WAS 0,38% FROM BOTTOMS UP (C1=3861 AND C2=2 PPM) MADE UP PACKOFF RUNNING TOOL AND RIH WHILE CIRCULATING." "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: CIRCULATED DOWN DRILL PIPE AND UP RISER AT 1050 LPM. MAX GAS WAS 0,26% FROM DEPTH OF WELL HEAD (C1=1969 PPM)" "On 1993-04-28, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: LANDED IN AND RETORQUED PACKOFF. RECIEVED ALL ROTATION BACK THAT IT TOOK TO TORQUE UP TO 15,000 FTLBS. CLOSED MPR, CHOKE LINE AND PRESSURE TESTED PACKOFF TO 345BAR/10MIN. OPENED MPR, TORQUED PACKOFF BACK UP TO 15,000 FTLBS. 1 INCH OF ROTATION DID NOT COME BACK WHEN TORQUE WAS RELEASED." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: CIRCULATED DOWN DRILL PIPE AND UP RISER AT 1050 LPM. MAX GAS WAS 0,06% FROM DEPTH OF WELL HEAD (C1=491 PPM)" "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 158m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: DISPLACED TO PACKER FLUID FROM 160M TO WELLHEAD." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH AND LAID DOWN PACKOFF RUNNING TOOL." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: RIGGED UP TO AND PULLED BOP. INSPECTED WITH ROV WHEN CONNECTOR WAS RELEASED, VX-RING WAS NOT LEFT ON TOP OF 18 3/4' HOUSING. SET ROP CAP ON TOP OF HOUSING. DID NOT OBSERVE ANY GAS FROM WELL AFTER PULLING BOP." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: SET ROV CAP ON TOP OF HOUSING. DISCONNECTED ALL GUIDEWIRES. DEBALASTED RIG 3,2M SO THAT BOP WAS 2M OVER TEMPLATE ROOF. RAN TV-WINCH TO TEMPLATE." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: ELECTRICAL ASSIGNMENT PROBLEMS IN SCR ROOM FOR ANCHOR WINCHES." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: PULLED OUT W/SCORPION ROV DUE TO PROBLEMS W/LEAKING HYDRAULIC HOSE. LAUNCHED SEA OWL ROV." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 0.5 hours. Operational details: MOVED RIG AND BOP 25 M OFF TEMPLATE IN DIRECTION 20 DEGREES." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: INSPECTED BOP-CONNECTOR FOR LOCATION OF VX-RING AND FOUND RING IN CONNECTOR. ACTIVATED VX-RING LOCKPINS SEVERAL TIMES AND REINSPECTED CONNECTOR. FOUND RING MISSING AND LOCATED SAME ON SEABOTTOM." "On 1993-04-29, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: LAUNCHED SCORPION ROV. PREPARED TO AND CLOSED HATCH COVER OVER SLOT S3." "On 1997-07-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 7.5 hours. Operational details: RIG MOVEMENT TO LOKE TEMPLATE 15/9" "On 1997-07-16, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 1.0 hours. Operational details: ON LOCATION. STARTED ANCHOR HANDLING. DROPPED ANCHOR #3" "On 1997-07-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 5.5 hours. Operational details: CONTINUED WITH ANCHOR HANDLING. ANCHOR #1 ON BOTTOM AT 0030 HRS - FAR SERVER. ANCHOR #10 ON BOTTOM 0040 HRS - NORMAN HUNTER. ANCHOR #7 ON BOTTOM 0220 HRS - FAR SERVER. ANCHOR #8 ON BOTTOM 0330 HRS - FAR SERVER. ANCHOR #4 ON BOTTOM 0500 HRS - NORMAN HUNTER. ANCHOR #11 ON BOTTOM 0530 HRS - RED ROOSTER" "On 1997-07-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 0.5 hours. Operational details: ANCHOR # 2 ON BOTTOM 0545 HRS - FAR SERVER ANCHOR # 11 ON BOTTOM 0600 HRS - RED ROOSTER" "On 1997-07-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 2.0 hours. Operational details: COMPLETED ANCHOR-HANDLING: NO. 5 ON BOTTOM 0615 HRS." "On 1997-07-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- transit' and lasted for 7.5 hours. Operational details: BALLASTED RIG DOWN TO DRILLING DRAFT." "On 1997-07-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- anchor' and lasted for 6.0 hours. Operational details: PRE-TENSIONED ALL ANCHORS TO 140 T. HAD TO RE-SET ANCHOR NO. 1." "On 1997-07-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: P/U THORT, R/U BOP TO TEST SPOOL AND RE-PERFORMED DUMMY RUN TO SET ORIENTATION." "On 1997-07-17, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.0 hours. Operational details: MOVED RIG 20 M TO STB AND RIGGED DOWN BOP SET UP." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- position' and lasted for 1.0 hours. Operational details: RIGGED DOWN BOP SET UP." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 5.0 hours. Operational details: PREPARED FOR REMOVING HATCH FROM SLOT S3. LOWERED RETR. FRAME DOWN ONTO TEMPLATE BY USING CRANE. RE-POSITIONED RIG WHILE REMOVING TWO LOCKING BOLTS FROM HATCH BY USING ROV. RAN ROV-HOOK/SLINGS ON DP. CONN. TO RETR. FRAME. WORKED TO ENGAUGE RETR. FRAME INTO HATCH." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: RETRIEVED PROTECION HATCH FROM SLOT S3. PARKED SAME ON TOP OF TEMPLATE STRUCTURE." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: CONNECTED GUIDE-LINES ON POSTS NO. 2 AND NO. 3, ASSISTED BY ROV. POOH W/ DP AND SLINGS. MOVED RIG OFF LOCATION." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: M/U CORROSION CAP RT ON DP." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.5 hours. Operational details: MOVED RIG OVER LOCATION." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 4.0 hours. Operational details: ATTEMPTED TO RETR. CORR. CAP ON DP. NEG. RAN RETR. TOOL ON TUGGER. RETRIEVED CORR. CAP ASSISTED BY ROV." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: MOVED RIG OFF LOCATION." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: P/U AND M/U FMC EMERGENCY HANGOFF TOOL. RACKED SAME IN DERRICK." "On 1997-07-18, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: P/U 5' DP WHILE PREPARING BOP." "On 1997-07-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 6.0 hours. Operational details: P/U 5' DP AND RACKED SAME IN DERRICK WHILE PREPARING/WORKING ON BOP: INSTALLED LATCH/UNLATCH INDICATOR ON BOP WH CONN. (FOR ROV VERIFIC.). PULLED YELLOW POD FROM LMRP RECEPTICLE AND INSTALLED PILOT LINES FOR ORIENTATION PIN OPERATION." "On 1997-07-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 8.0 hours. Operational details: P/U 5' DP WHILE PREPARING/WORKING ON BOP." "On 1997-07-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: R/U TO RUN BOP AND RISER." "On 1997-07-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: P/U AND M/U 2 X 50 FT RISER JOINTS." "On 1997-07-19, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 7.5 hours. Operational details: R/U TO RUN BOP: MOVED BOP FROM AFT POS. TO BELOW RT. MOVED LMRP FROM FWD POS. AND CONNECTED SAME TO BOP. DRESSED BOP W/GUIDE-LINES NO. 2 AND NO.3. FUNCTION TESTED BOP ON BOUTH PODS. CHECKED CONN. LATCH/UNLATCH. CHECKED FUNCT. OF ORIENTATION PIN (YELLOW POD). INST. BACON/SLOPE IND." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: HELD SAFETY MEETING PRIOR RUNNING BOP. RAN BOP AND RISER." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: P/U SLIP JOINT. M/U LANDING JOINT." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: INSTALLED KILL-/CHOKE-LINES." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: INSTALLED RUCKER RING ON RISER." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POSITIONED RIG OVER LOCATION." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: ORIENTED BOP/TEMPLATE. LANDED/LATCHED BOP ONTO 18-3/4' WH AT 0930 HRS. TOOK 25 T OP." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 5.0 hours. Operational details: CONN. HOSE SADLES AND POD REELS. RELEASED INNER BARREL. L/D LANDING JNT. INSTALLED DIVERTER. L/D RISER HANDLING TOOL. CHANGED BAILS AND ELEVATORS." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 2.0 hours. Operational details: M/U WB TO R/T. RIH. LANDED IN WH. PRESS. TESTED KILL-/CHOKE LINES AND BOP CONN. TO 345 BAR." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: ATTEMPTED TO SET WB. NEGATIVE. POOH." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: M/U AND RIH W/ JET SUB. WASHED AND CLEANED WH AREA. POOH." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: M/U BACK-UP WB TO R/T. RIH AND SET WB." "On 1997-07-20, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: P/U AND M/U 8-1/2' ROTARY DRILLING BHA. P/U DC'S AS RIH." "On 1997-07-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: CONT. M/U 8-1/2' BHA. TAGGED TOP CMT. AT 190 M (WASHED DOWN LAST STD)." "On 1997-07-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: DISPLACED WELL TO 1,38 SG BENTONITE MUD. FLUSHED KILL-/CHOKE LINES. RECORDED SCR. PERFORMED CHOKE-DRILL." "On 1997-07-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 215m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: DRILLED HARD CMT INSIDE 9-5/8' CSG FROM 190 M TO 215 M." "On 1997-07-21, at Well NO 15/9-19 S, a drilling event occurred at a depth of 356m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: DRILLED HARD CMT INSIDE 9-5/8' CSG FROM 215 M TO 356 M." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 402m. The activity was categorized as 'drilling -- drill' and lasted for 5.5 hours. Operational details: DRILLED HARD CMT INSIDE 9-5/8' CSG FROM 356 M TO 402 M. HIT 9-5/8' BRIDGE-PLUG AT 402 M." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 402m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: DRILLED ON 9-5/8' BRIDGE-PLUG AT 402 M." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 403m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: DRILLED OUT 9-5/8' BRIDGE-PLUG FROM 402 M TO 403 M." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 403m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: BROKE THROUGH 9-5/8' BRIDGE-PLUG. CLOSED UAP. CIRC. B/U THROUGH CHOKE- LINE. NO GAS." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3199m. The activity was categorized as 'drilling -- trip' and lasted for 8.5 hours. Operational details: RIH W/ 8-1/2' BIT FROM 403 M. P/U 81 JNTS 5' DP AS RIH. TOOK WT AT 3199 M (20 T)." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: MILLED 1 M W/ 20 T WOB. NO PROGRESS BELOW 3200 M, INDIC. TOP OF LINER AT 3200 M." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3200m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.0 hours. Operational details: CIRC. BU." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3000m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH W/ 8-1/2' BIT TO 3000 M." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: REPAIRED ON DP ELEVATOR." "On 1997-07-22, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1500m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: POOH W/ 8-1/2' BIT FROM 3000 M TO 1500 M. SCRAPED INTERV. 2190-2210 M SEVERAL TIMES (PLANNED BRIDGE-PLUG SETTING DEPTH)." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: CONT. POOH W/ 8-1/2' BIT FROM 1500 M. RACKED BHA IN DERRICK." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 1000m. The activity was categorized as 'plug abandon -- trip' and lasted for 3.0 hours. Operational details: P/U AND M/U 6 STD 3-1/2' CMT STINGER. RIH W/ SAME TO 1000 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3208m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.5 hours. Operational details: RIH W/ 3-1/2' CMT STINGER FROM 1000 M TO 3208 M. TOOK WT." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3208m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: WORKED MULE-SHOW THROUGH RESTRICTION IN 7' LINER LAP." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3309m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: CONT. RIH W/ 3-1/2' CMT STINGER FROM 3208 M TO 3309 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3309m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 2.0 hours. Operational details: CIRC. TO CONDITION MUD. DISPLACED HI-VIS PILL (1,38 SG) FROM 3309 M - 3259 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3259m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH W/ 3-1/2' CMT STINGER FROM 3309 M TO 3259 M. R/U TO CMT UNIT." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3259m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: SET A BALANCED CMT PLUG FROM 3259 M - 3109 M AS FOLLOWS: PUMPED 5 M3 FW SPACER, MIXED AND PUMPED 4,63 M3 1,92 SG CMT SLURRY. PUMPED 1,7 M3 FW SPACER BEHIND. DISPLACED PLUG W/ 26 M3 BENT. MUD." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH W/ CMT STINGER FROM 3259 M TO 3050 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 3050m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: REV. CIRCULATED STINGER VOLUM." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2800m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH W/ 3-1/2' CMT STINGER FROM 3050 M TO 2800 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2800m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 0.5 hours. Operational details: PLACED HI-VIS PILL FROM 2800 M TO 2300 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2300m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: POOH W/ 3-1/2' CMT STINGER FROM 2800 M TO 2300 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 1.0 hours. Operational details: PREPARED TO DISPL. WELL TO 1,50 SG ULTIDRILL MUD, CLEANED RIG-FLOOR." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2300m. The activity was categorized as 'plug abandon -- circulating conditioning' and lasted for 3.5 hours. Operational details: DISPLACED WELL TO 1,50 SG ULTIDRILL MUD FROM 2300 M." "On 1997-07-23, at Well NO 15/9-19 S, a drilling event occurred at a depth of 750m. The activity was categorized as 'plug abandon -- trip' and lasted for 2.0 hours. Operational details: POOH W/ 3-1/2' CMT STINGER FROM 2300 M TO 750 M." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: CONT. POOH W/ 3-1/2' CMT STINGER FROM 750 M. RACKED SAME IN DERRICK." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: R/U ATLAS WIRELINE." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: RIH W/ 9-5/8' BRIDGE-PLUG ON ATLAS WIRELINE. CCL QUIT WORKING. POOH. CHANGED OUT CCL." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: RIH W/ 9-5/8' BRIDGE-PLUG ON ATLAS WIRELINE." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 750m. The activity was categorized as 'interruption -- repair' and lasted for 2.0 hours. Operational details: ATLAS WIRELINE RIH WITH 9 5/8' BRIDGE-PLUG. CCL FAILED AGAIN AT 750M. POOH WITH BRIDGE-PLUG; OUT OF HOLE AT 0715 HRS. ATLAS REPAIRED CCL PROBLEM." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2200m. The activity was categorized as 'interruption -- repair' and lasted for 4.0 hours. Operational details: RIH WITH BRIDGE-PLUG ON ATLAS E/LINE TO 2200 M. ELECTRICAL PROBLEM PREVENTED BAKER SETTING TOOL FROM SETTING BRIDGE-PLUG. POOH WITH BRIDGE-PLUG; OUT OF HOLE AT 1140 HRS." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 8.5 hours. Operational details: ATLAS WORKED ON TROUBLESHOOTING PROBLEM WITH SETTING TOOL.RETERMINATED CABLE HEAD. FLEW SETTING TOOL FIRING HEAD OUT TO RIG; REPLACED SAME. ATLAS CHECKED TOOL & MU 9 5/8' BRIDGE-PLUG." "On 1997-07-24, at Well NO 15/9-19 S, a drilling event occurred at a depth of 2203m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: RIH WITH BRIDGE-PLUG ON E/LINE. LOCATED CASING COLLAR & SET TOP OF BRIDGE-PLUG 1,5 M BELOW COLLAR - AT 2203 M. POOH WITH E/LINE & SETTING TOOL. WITH B/S RAMS CLOSED, STARTED PRESSURING-UP ON 9 5/8' X 10 3/4' STRING WHILE RD ATLAS E/LINE." "On 1997-07-25, at Well NO 15/9-19 S, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: PRESSURE TESTED 9 5/8' CASING + BRIDGE-PLUG TO 345 BAR FOR 10 MINUTES." "On 2007-11-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 2.0 hours. Operational details: Held tool box meeting with involved personnel. Prepared equipment for skidding. Skidded rig from F-4 to F-14. Removed hatch on F-14." "On 2007-11-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 6.0 hours. Operational details: Continued changing wires on aft PRS. Meanwhile rigged tugger in moonpool for running DCI hose. Worked on releasing DCI hose connection. Came free at 19:00. Changed oil in TDS and cleaned pits. Stopped working on aft PRS due to high wind speed." "On 2007-11-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.0 hours. Operational details: Removed hatches and built scaffolding/fence around open hatches on all levels on slot F-14. Recovered tugger for DCI hose." "On 2007-11-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: LD 8 1/4' DC stand and jar." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: LD 8 1/4' DC stand and jar." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 5.0 hours. Operational details: WOW due to noe crane operation. Wind 45-50 knop, with gust up to 65 knop." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 4.0 hours. Operational details: WOW due to noe crane operation. Wind 40-45 knop, with gusts up to 60 knop. Meanwhile changed oil in TDS, adjusted fingerboard for CART stand, cleaned pits and carried on with rig maintenance." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.0 hours. Operational details: Changed wash pipe and serviced TDS." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 2.0 hours. Operational details: PU CART and MU to stand. RB in derrick." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- trip' and lasted for 4.2 hours. Operational details: PU 36' HO assembly. Removed master bushing and outer ring. RIH with 36' HO assembly to 9 m and re-instated outer ring and bushing. MU and RIH with 36' HO BHA from 9 m to 63 m." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Performed derrick inspection prior to spudding the hole. Special care were taken due to high winds of 40-50 knop." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 93m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: MU and RIH with 36' HO BHA from 63 m to 93 m." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 93m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Stopped RIH due to power syncronisation interference with production/prosessmodul." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 146m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: MU 36' BHA from 93 m to 143 m. Stung into funnel assisted by ROV. Observed fill in funnel and below. ROV had black-out on camera as soon as 17 1/2' bit had entered funnel. ROV went to surface for repairs. Continued RIH slowly without pumps and with no rotation until positive tag at 145.7 m." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 148m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Pumped SW at 550 lpm and washed down with no rotation to 148 m to allow centralizer drill bushing to land out in template guide-funnel." "On 2007-11-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 36' hole from 148 m to 150 m MD. Drilling parameters : Flow 550 lpm / SPP 4-5 bar / 5 RPM / Torque 1-2 kNm / WOB 1 MT. Reamed hole to ensure landing of centralizer drill bushing in template guide-funnel." "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 158m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled 36' hole from 150 m to 158 m MD. Drilling parameters : Flow 550-3100 lpm / SPP 4-40 bar / 5-20 RPM / Torque 2-4 kNm / WOB 1-2 MT / ROP 5 m/hr. Pumped 20 m3 hi-vis pill prior to connection. Downlinked and performed survey at 145 m. Survey at 145 m 0.3 inc" "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 193m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Drilled 36' hole from 158 m to 193 m MD. Drilling parameters : Flow 4550 lpm / SPP 80-82 bar / 90 RPM / Torque 4-10 kNm / WOB 1-6 MT / ROP 15-20 m/hr. Pumped 20 m3 hi-vis pills prior to connection. Downlinked and performed survey at 154, 164 and 174 m. Up weight 103 MT / Down weight 96 MT. Survey at 154 m 0.21 inc at 164 m 0,26 inc at 174 m 0,37 inc" "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 204m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 36' hole from 193 m to 204 m 17 1/2' bit depth / 201 m 36' HO depth. Drilling parameters : Flow 4550 lpm / SPP 80-82 bar / 90 RPM / Torque 4-10 kNm / WOB 1-6 MT / ROP 15-20 m/hr. Pumped 20 m3 hi-vis pills prior to connection. Downlinked and performed survey at 184 m. Survey at 184 m 0.43 inc" "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 204m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 25 m3 hi-vis sweep and circulated btms up with SW. Displaced hole to 1.40 sg bentonite mud, Flow 5000 lpm / SPP 140 bar / 30 RPM / Torque 2 kNm." "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: POOH with 36' HO BHA from 204 m to 150 m. Topped up hole with 1.40 sg bentonite mud. Continued POOH with 36' HO BHA from 150 m to 9 m." "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Removed master bushing and outer ring. POOH with 36' HO assembly and re-instated outer ring and bushing. LD 36' HO assembly." "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.8 hours. Operational details: WOW due to no crane operation. Wind 40 knop, with gusts up to 50 knop. Meanwhile serviced TDS, greased manifolds on BOP, K/C, stand pipe manifolds and performed fluid ends inspection on MP2." "On 2007-11-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Changed elevator and bails. Installed 30' bushing. Prepared HTS." "On 2007-11-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared rig floor." "On 2007-11-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Held pre-job meeting with all personnel involved. Prepared shoe joint and checked float for flow-through with SW. Painted shoe white. Continued to RIH with 30' conductor as per tally." "On 2007-11-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 30' conductor x-over joint and started installing cement top-up system with cement outlet 35 m below mud line. Aligned UWG top-up system to avoid conflict with the 3 hydraulic rams in the template well slot." "On 2007-11-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with 30' conductor x-over joint and installing cement top-up system with cement outlet 35 m below mud line." "On 2007-11-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 45m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Changed 30' conductor bails and elevator to to 5 1/2' DP handling equipment." "On 2007-11-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held pre-job meeting with involved personnel. Focused on weather conditions and running into splash zone. PU and installed 30' conductor housing joint." "On 2007-11-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 12.0 hours. Operational details: WOW, due to high wind and waves. Wind 50-87 knop." "On 2007-11-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WOW, due to high wind, waves and hael. Wind 65-83 knop." "On 2007-11-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: WOW due to high wind and waves." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: WOW due to high wind and waves." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 7.0 hours. Operational details: WOW. High wind and waves. Meanwhile performed rig maintenance." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held a tool box meeting. Run the 30' conductor housing. Laid down the conductor running tool." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Run and made up the cementing stinger in the conductor." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Picke up CART housing. Installed 2' fill up valve. Installed inclinometer on CART." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Installed top up cement system on the 30' conductor pipe whlie running down. Foot injury on centraliser deck." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Investigated incident involving a service hand." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued to install top up cement system on the 30' conductor pipe whlie running down." "On 2007-11-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Run 30' conductor on 5 1/2' landing string." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued to run 30' conductor on 5 1/2' landing string. Problems with top drive torque wrench." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 55m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Problems with torque wrench on top drive. Not able to disconnect top drive from landing string." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 169m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pulled back one single. Broke connection using the iron roughneck. Continued to RIH. Stabbed conductor into guide funnel at 03:30 hrs. Checked orientation of conductor shoe. Observed a broken connetion on the top up cement system. Continued to run the conductor to 160 m. Observed 20 tons weight. Worked conductor down to 169 m." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 169m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Made up the top drive and started to wash down from 169 m. Flow: 1000 ltr/min. SPP: 4 bar. Observed some of the cement top up piping no longer attached to the conductor pipe. Attempted to recover broken cement top up piping in the guide funnel." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 169m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Recovered broken off piece of top up cement piping." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 180m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box meeting with oncoming crew. Washed down with 30' conductor from 169 to 180 m, 1000 lpm." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 190m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Held a toolbox meeting. Rigged up tugger on centralizer deck and pulled conductor to starboard aft. Guided the conductor carefully through the guide funnel to 180.2 m to avoid further damage on top up cement piping. Washed down with 30' conductor from 180.2 m to 190 m, 1000 lpm. Observed leakage in top up cement piping at approx. 11 m below top housing." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Laid down top single at 190 m. Made up the cement stand. Washed down with the conductor to approx 40 cm above TD, 1000 lpm. Took digiquartz measurements. RIH and set conductor at TD 196.8 m. Confirmed top of housing 43 cm lower than F-7." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Prepared to activated the centralizers on the template using the ROV." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 199m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Held a tool box meeting regarding the cementing of the 30' conductor. Pressure tested the cementing line to 100 bar. Connected hot stab. Run centralizer sylinders on template and verified conductor position with ROV. Checked inclination: Roll 0.12, pitch 0.8." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Circulated 30 m3 of SW with 2500 lpm. Observed returns from slot F-14 came out of conductor annulus on slot F-7. Took time out, evaluated situation." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held a tool box meeting prior to rig down the cement line." "On 2007-11-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 196m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Retracted centralizer dogs on template. Picked up 0,5 m to confirm conductor free, free up weight 124 ton, no excess drag." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Attempted to confirm dogs fully retracted with ROV, not possible due to bad visibility." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 196m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW for visibillity to improve on the template." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Washed back to TD with conductor, 800 lpm." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.5 hours. Operational details: WOW for visibility to improve on template." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 15.5 hours. Operational details: WOW for visibility to improve on template. Unable to engage hot-stab for centraliser rams. Damaged claw for ROV arm. Came to surface with ROV to repare claw, dived again with ROV." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW for visibility to improve on template. Held meeting with essential personnel and went thought conductor cementing procedure." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 1.2 hours. Operational details: WOW for visibility to improve on template." "On 2007-11-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.8 hours. Operational details: WOW for visibility to improve on template. Meanwhile lined up and pressure tested the cement line to 100 bars. Stabbed hot-stab." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Worked with centralizer rams, rams were not working properlyy. Took out the hot-stab and flushed the lines, and stabbed the hot-stab back in, now the centralising rams worked properly. Retracted rams." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: WOW for visibility to improve on template." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to cementing of the 30' conductor." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Circulated SW at 250 lpm increased to 1000 lpm in 250 lpm steps. Still only returns coming out from F-7, hook load came down with 10 MT to 92 MT while pumping at 1000 lpm." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Pumped 30 m³ 1.7 SG mud, 1000 lpm, 5.7 bars, hookload dropped to 85 MT. Still only returns out from F-7. Picked up one meter with 120 MT and washed conductor back to setting depth, final hook load 76 MT. Total 20 m³ 1.7 SG mud pumped while washing down." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Started to take digiquartz measurement to confirm correct setting depth of the 30' conductor." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Picked up to original pick up weight of 120 MT 0.8 meter. Washed down conductor to correct setting depth at 196.8 meter, hook load 101 MT. Checked depth with digiquartz; 38 cm below F-7. Pumped 19 m³ of 1.7 SG mud, then 38 m³ sea water while washing down, return fluid up on nearby well, F-7." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Washed down 5 cm, and circulated/worked string until correct hookload, pumped a total of 216 m³ of sea water. Hook load 101 MT. Return fluid up on nearby well, F-7." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Closed the centraliser Rams and verified same with the ROV. Checked depth with digiquartz; 43 cm below F-7." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped 15 m³ 1.65 SG mud and applied 20 bars back pressure to IBOP." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Mixed and pumped 106 m³ 1.52 SG Tuned Light XL cement slurry, experienced problems with plugged lines towards the end. Pumped first 20 m3 at 600 lpm, then increased rate to 1000 lpm. Checked returns on F-7, only minor returns after 70 m³ pumped, got returns up F-14. Displaced cement slurry with 6.5 m³ SW with mud pumps. Hook load dropped from 101 to 99 MT during cement job." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Bled off pressure and checked for back-flow. Removed cement hose and flushed through manifolds and hoses." "On 2007-11-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 6.8 hours. Operational details: Waited on cement to set. Meanwhile performed general maintenance." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Waited on cement to set. Meanwhile performed general maintenance." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to pressure test of top-up system." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up for flushing of top-up line." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Flushed top-up system and surface lines. Pressure tested UWG top-up system using the cement unit, rupture disk burst at 53 bars (769 psi)." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Opened centralizer rams on F-14. Retrieved the hot stab from bank # 4." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk prior to perform top-up cement job." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Started to circulate with sea water 500 lpm. Performed cement top-up job, pumped 10.4 m³, 1.56 SG G-cement 82 bars at 500 lpm." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Flushed cement lines. Dropped 24 mm ball into the top-up hose, applied 240 bars to top-up to release the line NO-GO, bled down the pressure. Cut the hose using the ROV. Flushed lines and manifold on the rig floor and cement unit." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Checked inclinometer reading on the CART, opened the valve on the CART tool. Released the CART tool, slacked off to neutral weight = 76 MT, turned to the right 400/3000 Nm. Picked up the CART, tool weight 79 MT. Laid out the cement pump in sub." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box prior to laying out the landing string. Laid out pup jnts. and HWDP landing string and checked serial numbers. Measured length using a laser measure, racked back landing string in derrick." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Problems with the PRS investigated same." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 167m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued POOH with landing string, measured same with laser." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 167m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Due to unusual noise from forward PRS, stop operation and performed full inspection of same." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued POOH with landing string, measured same with laser." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pull the master bushing, removed same. Pulled out the CART tool and removed the inclinometer, installed the master bushing." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Function tested and preserved the CART tool." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk, prior to measuring the landing string, and laying out the aluminium inner string." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleaned the rig floor." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Prepared for measuring the double on top of the CART tool. Laser measuring device was drop down onto the rig floor" "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Operation was terminated and an investigating was established. A statement of the incident was put together." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk, prior to measuring the landing string, and laying out the aluminium inner string. Measured the double." "On 2007-11-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Racked back the CART tool in derrick. Laid out the aluminium inner string." "On 2007-11-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 4.5 hours. Operational details: Prepared for skidding of the cantilever from F-14 to F-5" "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 3.0 hours. Operational details: Held toolbox talk prior to skidding rig from F-1 to F-14. Skidded rig 3 m starboard. Skidded rig/cantilever 6,5 m aft. Removed hatches in wellhead module on F-14. Ran stand of HWDP through rotary and made final adjustments." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Broke down stand of 5 1/2' HWDP and laid out three joints for backload and inspection. Rebuilt stand with 3 new joints of 5 1/2' HWDP and racked back in derrick. Ran tugger from moonpool to seabed to help ROV clear CTS hose." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Picked up 26' drilling BHA and brought to V-door. Meanwhile helped ROV to clear hose trapped below template using tugger." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 22m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Held toolbox talk prior to making up 26' drilling BHA. Removed masterbushing and ran 26' Bit / gMWD assy through rotary. Inserted gMWD probe in BHA as per Scientific instructions. Meanwhile ROV attempted to connect hose to CTS funnel. CTS hose was too short and the funnel had to be turned. ROV lost 3-finger claw when attempteing to turn CTS funnel." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Continued running BHA. Picked up and made up MWD/UBHO assy. Meanwhile pulled ROV to surface for repair." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 33m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Orientated UBHO sleeve as per Scientific instructions. Meanwhile repaired ROV manipulator claw." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Made up 3 x 9 1/2' NM DC to BHA and ran in to 63 m MD. Repaired ROV and launched same. Assessed video recording from incident. Found 3-finger claw to be lost in hole. Assessed situation." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Laid out 1 x DC and made up hydro- mechanical jar to 8 1/4' DC stand. Racked back in derrick. Discussed way forward with town." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 63m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Awaited further instuctions. Discussed way forward with town. Decided to run in with 26' rock bit BHA in attempt to remove junk in hole." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.2 hours. Operational details: POOH with 26' drilling BHA. Racked back BHA in derrick. Laid out UBHO/MWD assy on deck." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up new 26' junk removal BHA with rock bit." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made up 26' bit and bit sub to stand of 9 3/4' drillcollars. Removed masterbushing, ran stand through, installed masterbushing and hung off assy in rotary table." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made up jar and 8 1/4' DC stand. Picked up single 8 1/4' DC and made up same." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 26' junk removal BHA on 5 1/2' HWDP from 70 m MD to 175 m MD. Stabbed into CTS on top of conductor housing while observing with ROV." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 183m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Washed down from 175 m to 183 m MD with 1000 lpm and tagged cement with 5 MT. Applied 4-6 MT WOB and rotated at 15 rpm down to 185 m MD." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: POOH with 26 junk removal BHA from 185 m to just above CTS funnel at 138 m MD. ROV inspected 26' rock bit. No damage or junk could be observed." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 185m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Ran back in to 185 m MD to resume drilling cement. Connected CTS hose to ROV and started pumping with dredge pump." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 197m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Drilled cement from 185 m to 197 m MD. Drilling parameters : Flow 4400 lpm / SPP 62 bar / Rotation 45 rpm / Torque 1-3 kNm. Controlled penetration rate to 15 m/hrs. Observed higher WOB (autodrill 15 m/hr) from 193 m to 197 m MD indicating hard cement. 20 MT tonne WOB peak at 193 m MD and 3-10 MT downwards. Observed excessive rattling in string and WOB peaks around shoe depth at 197 m MD. Pumped 2 x 20 m3 hi-vis sweeps to clean hole." "On 2007-12-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 201m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled rathole and shoe from 197 m to 201 m MD. Drilling parameters : Flow 4400 lpm / SPP 62 bar / Rotation 45 rpm / Torque 1-2 kNm / WOB 1-2 MT. Reamed back inside shoe for every 2 m drilled." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 204m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Drilled rathole and shoe from 197 m to 201 m MD. Drilling parameters : Flow 4400 lpm / SPP 62 bar / Rotation 45 rpm / Torque 1-6 kNm / WOB 1-8 MT. Reamed back inside shoe for every 2 m drilled." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 206m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 2 m new formation from 204 m to 206 m MD. Drilling parameters : Flow 4400 lpm / SPP 62 bar / Rotation 45 rpm / Torque 1-2 kNm / WOB 1-2 MT. Pumped 20 m3 his-vis sweep to clean hole." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 3.0 hours. Operational details: POOH with 26' junk removal BHA from 206 m MD to surface on 5 1/2' HWDP. Laid down 1 x 8 1/4' DC. Racked back jar/DC assy. Lifted UBHO/MWD assy to HTS due to wind speed limitations on crane. Pulled 9 3/4' DC/bit stand to surface and inspected 26' rock bit. Found 2 x pieces of junk trapped in roller cones. Removed 1 piece of 800 g. The other piece was jammed in middle of the bit and could not be removed easily. Also found several worn teeth on bit." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Broke 26' bit and bit sub. Racked back stand of 9 3/4' DC." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 70m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Ran 26' drilling BHA from surface to 70 m MD." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 133m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Ran 26' drilling BHA from 70 m to 133 m MD." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 206m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: RIH with 26' drilling BHA from 133 m to 206 m MD. Stabbed into CTS funnel while observing with ROV." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 211m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Established drilling parameters. Drilled 26' hole section from 206 m to 211 m MD. Drilling parameters : Flow 3100 lpm / SPP 62 bar / 1-2 MT WOB / Rotation 125 RPM / String torque 1-3 kNm. Pumped 20 m3 hi-vis to clean the hole at 211 m MD. Scientifc drilling reported that UBHO sleeve had not been fastened correctly in the carrier. Decided to pull BHA for remedial action." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 63m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: POOH with 26' drilling BHA from 211 m MD to 63 m MD. No drag observed when pulling BHA through conductor shoe. Racked back DC/jar and NMDC stands to access UBHO sub." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 63m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Checked UBHO relative to scribeline. Checked and thightened UBHO sleeve. Inspected 26' bit at Centralizer deck - no wear observed." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 196m. The activity was categorized as 'interruption -- repair' and lasted for 2.5 hours. Operational details: Made up and RIH with 26' drilling BHA from 63 m to 196 m MD. Stabbed into CTS funnel while observing with ROV." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 209m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Washed down with 26' drilling BHA from 196 m to 209 m MD pumping at 2000 lpm." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 195m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: Performed singel shot survey on WL with bit inside conductor shoe. Inclination 0,33 deg / Azimuth 306,1 deg / Toolface 050 deg. Halted drilling operation for software upgrade on Siemens F&G system." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 195m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Stand-by for software upgrade of Siemens F&G system. At 18:15 hrs => Washed down to 209 m MD while pumping at 2000 lpm. Shut down pumps and waited for gMWD to reset." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 209m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Pumped at 2000 lpm and obtained gMWD survey - rejected survey." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Slided 26' drilling BHA from 211 m to 217 m MD. Drilling parameters : Flow 3100 lpm / SPP 62 bar / 1-3 WOB / Rotation 95 RPM (bit rpm) / String torque 0-1 kNm. Pumped 10 m3 hi-vis sweep. Picked off bottom and hung off on slips." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 215m. The activity was categorized as 'drilling -- survey' and lasted for 1.2 hours. Operational details: Performed single shot survey on WL. Inclination 0,2 deg / Azimuth 243,9 deg / Toolface 112 deg. Pumped at 2000 lpm to obtain gMWD survey - rejected data." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Slided 26' drilling BHA from 217 m to 226 m MD. Drilling parameters : Flow 3100 lpm / SPP 62 bar / 2-6 WOB / Rotation 95 RPM (bit rpm) / String torque 0-1 kNm. Pumped 10 m3 hi-vis sweep. Picked off bottom and hung off on slips." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 226m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Performed single shot survey on WL. Inclination 0,37 deg / Azimuth 297,4 deg / Toolface 112 deg. Pumped at 2000 lpm to obtain gMWD survey - rejected data." "On 2007-12-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 233m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Slided 26' drilling BHA from 226 m to 233 m MD. Drilling parameters : Flow 3100 lpm / SPP 62 bar / 2-6 MT WOB / Rotation 95 RPM (bit rpm) / String torque 0-1 kNm." "On 2007-12-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 239m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued sliding from 233 m to 239 m MD. Pumped 10 m3 hi-vis sweep. Picked off bottom and hung off in slips." "On 2007-12-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 239m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Performed single shot survey on WL. Inclination 0,25 deg / Azimuth 320,5 deg / Toolface 125 deg. Adjusted toolface to 114 deg. Secured drillstring using chain hoist on Centralizer deck. Pumped at 2000 lpm to obtain gMWD survey - obatined data but still 16 deg deviation on toolface." "On 2007-12-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Slided 26' drilling BHA from 229 m to 249 m MD. Drilling parameters : Flow 3100 lpm / SPP 68 bar / 8-10 MT WOB / Rotation 95 RPM (bit rpm)/ String torque 1-3 kNm. Pumped 10 m3 hi-vis sweep. Picked off bottom and hung off in slips." "On 2007-12-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 249m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Performed single shot survey on WL. Inclination 0,27 deg / Azimuth 334,1 deg / Toolface 076 deg. Secured drillstring using chain hoist at Centralizer deck. Pumped at 2000 lpm to obtain gMWD survey : Inclination 0,44 deg / Azimuth 024,1 deg / Toolface 076 deg - good match on toolface figure. Good match between realtime GTF and MTF." "On 2007-12-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 259m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Slided 26' drilling BHA from 249 m to 258 m MD. Drilling parameters : Flow 3100 lpm / SPP 68 bar / 1-3 MT WOB / Rotation 95 RPM (bit rpm)/ String torque 0-2 kNm." "On 2007-12-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 269m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Drilled 26' hole section from 258 m to 269 m MD. Drilling parameters : Flow 3100 lpm / SPP 68 bar / 1-3 MT WOB / Rotation 130 RPM (bit rpm) / String torque 6 kNm." "On 2007-12-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 530m. The activity was categorized as 'drilling -- drill' and lasted for 18.0 hours. Operational details: Drilled 26' hole section from 269 m to 530 m MD. Drilling parameters : Flow 3100-4400 lpm / SPP 68-125 bar / WOB 2-8 MT / Torque 1-11 kNm / String RPM 40 / Bit RPM 40-170. Average ROP 15 m /hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Secured drillstring with sling/chainhoist on Centralizer deck while performing survey. Steered intervalls : 268 - 287 m MD 315 - 331 m MD 356 - 377 m MD 396 - 411 m MD 435 - 450 m MD 475 - 495 m MD 515 - 535 m MD" "On 2007-12-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 636m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 26' hole section from 530 m to 636 m MD. Drilling parameters : Flow 4400 lpm / SPP 125-127 bar / WOB 6-8 MT / Torque 2-8 kNm / String RPM 40 / Bit RPM 40-170. Average ROP 18 m /hrs. Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections. Secured drillstring with sling/chainhoist on Centralizer deck while performing survey. Steered intervalls : 555 - 575 m MD 597 - 615 m MD" "On 2007-12-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 878m. The activity was categorized as 'drilling -- drill' and lasted for 15.5 hours. Operational details: Drilled 26' section in rotation mode, from 636 m to 878 m MD. Drilling parameters : Flow 4400 - 4480 lpm / SPP 125 - 127 bar / WOB 6-10 MT / Torque 9 - 10 kNm / String RPM 40 / Bit RPM 165 - 172. Avarage ROP 20,3 m/ hrs.Pumped 10 m3 hi-vis sweep for every singel drilled. Performed gMWD survey on connections." "On 2007-12-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 981m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 26' section in rotation mode, from 878 m to 981m MD. Reduced flow-rate from 4480 lpm to 4000 lpm due to Utsira sand. Hit top of utsira sand at 888 m. Drilling parameters : Flow 4000 lpm / SPP 121 bar / WOB 2 - 5 MT / Torque 3 - 5 kNm / String RPM 40 / Bit RPM 160- 162. Avarage ROP 38,1m/ hrs. Pumped 10 m3 hi- vis sweep for every singel drilled. Performed g MWD survey on connections" "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1064m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 26' section in rotation mode, from 981 m to bottom of Utsira sand at 1064 m MD. Drilling parameters : Flow 4000 lpm / SPP 121 bar / WOB 2 - 5 MT / Torque 3 - 5 kNm / String RPM 40 / Bit RPM 160- 162. Avarage ROP 41,5 m/ hrs. Pumped 10 m3 hi- vis sweep for every singel drilled. Performed g MWD survey on connections." "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 26' hole from 1064 m to Td for section at 1083 m MD. Drilling parameters : Flow 4410 lpm / SPP 154 -156 bar / WOB 8 - 13 MT / Torque 10 -13 knm / String RPM 40 / Bit RPM 170. Avarage ROP 22,8 m/ hrs.Pumped 10 m3 hi.vis sweep for every singel drilled. Performed g MWD survey on connections." "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1083m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: At TD, pumped 30 m3 hi vis followed by 30 m3 sea watwr and then 55 m3 hi - vis. Reduced flow rate to 3500 lpm while pumping hi vis pill through BHA. Circulated hole clean with 4480 lpm / SPP 127-130 bar /String RPM 40 / Torque 3-4 kNm. Kept bit below Utsira sand during circulation / reciprocation." "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1072m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Displaced well to 1.40 sg bentonite mud with 3500 lpm / SPP 70 bar / String RPM 20 / Torque 1-4 kNm. Kept bit below Utsira sand during displacment. SPP leveled out after 14500 strokes at 3500 lpm / SPP 152 bar /String RPM 180 / Torque 2-4 kNm. Observed some returns coming through cement ports on 30' conductor on F-4." "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 717m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: POOH with 26' drilling BHA from 1072 m MD to 717 m MD. Tight spots when POOH: 807-800 m: 10-15 MT overpull 770-764 m: 13-16 MT overpull 758-754 m: 10-14 MT overpull 725-720 m: 16-21 MT overpull Encountered leak on PS21 slips." "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 717m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Discovered leakage on PS 21 slips. Changed hose." "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 193m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: POOH with 26' drilling BHA from 717 m MD to 193 m MD. Tight spots when POOH: 627-620 m: 2-10 MT overpull 615-612 m: 5-15 MT overpull 598-596 m: 11-20 MT overpull 595-590 m: 10-30 MT overpull 585-580 m: 15-30 MT overpull 578-575 m: 5-15 MT overpull" "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 193m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Built scaffolding under centralizer deck on well head module. Meanwhile topped up well with 1.40 sg mud at 193 m MD. Serviced TDS and PRS and performed derrick inspection for loose items." "On 2007-12-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 8.0 hours. Operational details: Held tool box meeting before manual handling of BHA. Continued POOH with 26' drilling BHA from 193 m MD to OOH. ROV guided BHA out of template. Flushed string with SW when bit was above template. Clean and cleared rig floor of excess equipment." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: LO pup joints on top of landing string. PU one joint HWDP. MU and RB cmt stand" "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Spotted csg handling equipment on rig floor." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held pre-job meeting prior to handling DCI valve. Brought DCI frame down to scaffolding below centralizer deck through rotary and deck openings using tugger. Hung up and chained back DCI frame from well head centre using chain hoists and eagle clamps." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RU casing running equipment, 20 ft bails and FAC tool." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 5.5 hours. Operational details: RU casing running equipment, 20 ft bails, elevators, csg tong, slips and FAC tool." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held pre-job meeting prior to running 20' csg. PU 20' shoe joint. Encountered signal problems to casing tong." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot ZMS signals on csg tong." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued PU 20' csg shoe assy. Encountered problems with FWD PRS & HTS" "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 12m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshoot signals and alignement on FWD PRS and HTS." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 39m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: PU intermediate joint and float collar joint. Tread locked connections. Checked float in shoe and float collar for flow through with SW. Filled each joint with 90 strk SW." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: RIH with 20' csg from 39 m to 109 m MD. Installed csg centralizers on each joint. Filled every joint with 90 strk SW. Average running speed 2 jnts/hr. Back-up chain on upper casing tong broke-off." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 109m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Back-up chains on upper part of casing tong broke off. Made up temporary solution with wire slings acting as back-up security to the counterbalance." "On 2007-12-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 151m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RIH with 20' csg from 109 m to 151 m MD. Installed one centralizer on each joint. Filled every joint with 90 strk SW. Average running speed 2 jnts/hr. Stabbed csg into conductor assisted by ROV. Had to use chain tongs in well head area to limit csg string movement in 3-4 m waves." "On 2007-12-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 414m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 20' csg from 151 m to 414 m MD. Filled string with SW every 5th joint. Average running speed 4 jnts/hr. Observed tight spots at: 250-256 m: 12 MT drag 282-293 m: 16 MT drag - circulated w/SW 650 lpm / 25 bar" "On 2007-12-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 923m. The activity was categorized as 'drilling -- casing' and lasted for 12.5 hours. Operational details: RIH with 20' csg from 414 m to 923 m MD. Filled string with SW every 5th joint. Average running speed 5 jnts/hr. Upweight 188 MT/down weight 144 MT at last joint before WH housing. Observed tight spots at: 576-588 m: 20-25 MT drag 701-738 m: 15-18 MT drag 800-825 m: 12-15 MT drag" "On 2007-12-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 923m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Greased slips prior to elevator change and topped-up casing with SW." "On 2007-12-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 923m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: RD 20' csg handling equipment and RU 5 1/2' handling equipment." "On 2007-12-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 923m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: PU 18 3/4' WH housing/CART assembly and MU to 20' casing. Oriented DCI valve outlet swivel to STB side using a ring bolt." "On 2007-12-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 934m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 18 3/4' WH housing/CART assembly from 923 m to 934 m. Removed PS30 slips and installed outer ring and master bushings." "On 2007-12-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 934m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RD csg tong and flush mounted elevators." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 934m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued RD csg tong and flush mounted elevators. Cleared rig floor." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 953m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 18 3/4' WH housing/CART assembly from 934 m to 953 m. Observed 20 MT drag. Circulated with 450 lpm / 30 bar and washed down." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 965m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Removed gas sensor and section of grating on x-mas tree deck to enable safe passage of WH housing through deck. Continued RIH with 18 3/4' WH housing/CART assembly from 953 m to 965 m." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 965m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held tool box talk prior to installing DCI valve. Installed DCI frame on 18 3/4' WH housing working on scaffolding platform below WH module." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 965m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Installed DCI frame on 18 3/4' WH housing working on scaffolding platform below WH module. Pressure tested DCI frame/ WH to 210 bar/ 5 min. Meanwhile held pre-job meeting for cement job." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1065m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Continued RIH with 20' casing on landing string from 965 m to 1065 m. Washed down last 10 m 440 lpm / 38 bar. Upweight 188 MT/ down weight 138 MT." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Landed 18 3/4' WH into 30' conductor by setting down casing string weight + 5 MT to engage lock ring. Performed 25 MT overpull test. Slacked off and kept landing string in tension by an overpull of 3 MT." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Established circulation in steps with SW to 2300 lpm. At 2000 lpm / 65 bar the returns broke through on well F-12. Reduced flow to 200 lpm / 27 bar and observed for 15 min. Continued circulating 320 m3 of SW at 2300 lpm with returns on F-12. Kept landing string in tension by an overpull of 3 MT." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up to pump from cement unit. Pressurized TDS to 31 bar and tested line up. Released 1 3/4' preloaded ball for bottom wiper plug." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Mixed and pumped 242 m3 1.52 sg lead slurry at 1180 lpm / 20 bar." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Mixed and pumped 20 m3 1.92 sg tail slurry at 800 lpm / 16-20 bar." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released top dart. Displaced and sheared sub sea wiper plug by pumping 3 m3 SW with cement unit at 1100 lpm / 11 bar. Top plug sheared after 880 ltrs / 190 bar." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Zeroed counters for mud pumps and lined up to displace cement with SW using mud pumps. Displaced cement with SW at 3000 lpm. Slowed down to 1400 lpm after 7157 stks (156.95 m3). FCP was 48 bar. Bumped plug after 7230 strokes with 93 bar. Last 20 min of displacement the returns came up F-14 and no flow was observed on F-12." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Bled of pressure and checked for backflow to cement unit. Volume bled back was 1100 ltr. Disconnected cement hose after pressure had been bled off." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Reduced overpull on landing string to neutral. Released CART by 5 right hand turns and observed wellhead with ROV. Pulled above top of wellhead." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Pumped 2 sponge balls and flushed landing string with SW. POOH with 18 3/4' CART from 140 m to surface. LO same." "On 2007-12-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: LO cement head. Prepared for skidding to F-9. Operation transfered to F-9." "On 2008-04-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.2 hours. Operational details: Held tool box talk and skidded cantilever to F-14" "On 2008-04-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Held tool box talk and prepared & rigged up HPDR spider and handling equipment for running HPDR. Function tested Spider slips." "On 2008-04-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box talk and picked up HPDR Tieback connecter, inspected same. Picked up HPDR double 'A' and made up same." "On 2008-04-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to run HPDR." "On 2008-04-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Completed making up HPDR double 'A'. Made up fairing protector." "On 2008-04-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Function tested HPDR TBC." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Continued function test of HPDR TBC. Running of HPDR suspended. Resumed maintenance of the aft PRS." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Pulled back the HPDR double 'A' and the TBC to rig floor. Held tool box talk prior to re-arranging hatch covers. Transferred riser equipment from the moon pool to the rig floor and to the tension deck. Picked up damaged tension cylinder from centraliser deck to rig floor. Prepared for skidding." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Held tool box talk prior to skid cantilever. Started to shut down production." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded the cantilever to F-12." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Prepared for re-arrange hatch covers." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Held tool box talk and moved hatches in the moon pool." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Held tool box talk and skidded cantilever from F-12 to F-14." "On 2008-04-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Installed guide wires for running the HPDR." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Continued installation of guide wires." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Ran in with TBC and HPDR double 'A'." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: ROV installed guide wires at template." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Made up 5½' DP to HPDR lifting sub, and racked back in derrick." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up HPDR double 'B'." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up HPDR 'B'. Removed lifting sub on HPDR 'A' and commenced preparing flange connection." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 8.8 hours. Operational details: Continued making up the HPDR and ran in same. Held tool box talk with day shift prior to run HPDR. Prepared ROV for brush & clean the VX profile on 18 3/4' WH and performed same." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up 5½' DP with HPDR lifting sub. Attached to the HPDR tension jnt. Ran in and parked TBC inside guide funnel" "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: ROV removed guide wires and funnel and parked funnel on F-3. Simultaneously prepared all equipment for installation of the tension system." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Landed riser and set down 22MT. Launched hot stab in moon pool and locked the TBC. Took over pull of 15 MT. Slacked off to 10 MT over pull." "On 2008-04-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Installed centralizer and Boat collision stool." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Installed tension ring, cylinders and the tensioning up system." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Applied 90 bars to the tension cylinders, equal to 150 MT." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Disconnected the HPDR lifting sub and retrieved same to the rig floor." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Laid out riser spider and installed master bushing. Prepared for installation of hatch covers." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed hatch cover on F-13 & F-15. Found that tension system not filled with Nitrogen." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'interruption -- repair' and lasted for 3.0 hours. Operational details: Held tool box talk and ran in with the HPDR lifting sub and made up same. Released hydraulic pressure to the tension cylinders and kept 132 MT on the string. Filled damper tank with Nitrogen. Applied 90 bars hydraulic pressure to the tension cylinders = 150 MT. Disconnected the HPDR lifting sub and retrieved same to rig floor." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Held tool box talk and ran in with BOP riser jnt and landed same. Secured hatch and made up the BOP riser jnt to the HPDR tension jnt." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Held tool box talk and lined up kill and equalized F-12 flow line for opening up production." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Completed making up the BOP riser jnt. Cleared the well bay area." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Filled up riser with SW and performed integrity test of the HPDR to 30 bars / 10 min." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Cleared well area for Vetco equipment. * Continued programmed maintenance of the aft PRS." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Prepared equipment for nippling the BOP. * Continued programmed maintenance of the aft PRS." "On 2008-04-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Built scaffolding around the BOP riser. * Continued programmed maintenance of the aft PRS." "On 2008-04-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Released the Claxton tool. Pulled out and LD 5½' DP." "On 2008-04-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Retrieved Claxton tool and parked it on the rig floor." "On 2008-04-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Held tool box talk and commenced nippling up the BOP." "On 2008-04-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Nippled up the BOP." "On 2008-04-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Installed bell nipple, diverter and made up bell nipple and torqued up NT2 connector. * Continued with planned maintenance in derrick and on PRS's." "On 2008-04-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held tool box and filled BOP/riser with SW. Performed line test to 155 bars 10 min." "On 2008-04-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pressure tested the well/BOP/riser to 155 bars 10 min. Volume pumped/return 1700/1500 litres. * Operation suspended due to programmed maintenance in derrick and PRS's" "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 35m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held toolbox talk for picking up 18 3/4' test plug. Picked up jet sub and hung off in rotary. Made up 5 1/2' stand. Installed elevator tilt on bails. Made up 18 3/4' test plug." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH with jet sub and 18 3/4' test plug on 5 1/2 DP to 136 m MD." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 144m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Stepped up pumps to 3100 lpm / SPP 30 bar. Reciprocated pipe and made 3 passes accross wellhead while pumping. Pumped a total of 46 m3 seawater." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Landed 18 3/4' test plug in wellhead at 140,9 m MD. Flushed lines and lined up cement unit to pump in kill line on BOP. Closed BOP." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 170m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: Pressure tested BOP connector to 20/345 bar 5/10 min. Observerd 0,61% drop on high pressure test, but trend improving with time - ok. Pumped and bled back approx 440 litres." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: POOH with jet sub / 18 3/4' test plug from 170 m MD to surface. Broke out and laid down 18 3/4' test plug and jet sub. Broke out and laid down 10 3/4' Itco spear while tracing extension for link tilt." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleared and tidied drillfloor. Made up nominal seat protector to running tool." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to running nominal seat protector." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: RIH with nominal seat protector on 5 1/2' DP from surface to 140 m MD. Set nominal seat protector at 140,8 m MD according to Vecto procedure." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with nominal seat protector RT from 140 m MD to surface. Reset running tool and laid out same." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Tested zone management system / anti collison for fwd PRS, aft PRS, TDS and IR - ok." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Cleared and cleaned drillfloor prior to bringing in 17 1/2' drilling BHA." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to making up 17 1/2' BHA." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- trip' and lasted for 6.5 hours. Operational details: Made up 17 1/2' drilling BHA comprising of Powerdrive X5, ARC, PowerPulse and SonicVison. Made up NMDC using manual tongs due to short x-over on SonicVision. Made up DC stand with hydraulic jar. Made up stand of DC. Made up 6 5/8' reg x 5 1/2' FH x-over. Made up stand of 5 1/2' HWDP." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 150m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Removed bowl and masterbushing. Installed PS-30 automatic slips." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1010m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: RIH with 17 1/2' drilling BHA on 5 1/2' DP from 150 m to 1010 m MD." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1038m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Lined up mudpumps. Stepped up pumps in increments to 3100 lpm / SPP 72 bar. Routed returns through dump hose on flowline. Observed overflow in moonppol due to unfavourable distribution of dump hose. Re-arranged dump hose with ropes and managed to stop overflow. Tested MWD telemetry - ok. Washed down to 1038 m MD while rotating at 30 RPM, no drag observed." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1048m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Picked up and made up 5 1/2' DP singel to be able to drill shoetrack and ratehole without making connection. Washed down with 3100 lpm / 30 PRM and tagged firm cement at 1048 m MD." "On 2008-05-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1050m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Drilled firm cement from 1048 m to 1050 m MD. Drilling parameters : Flow 3100 lpm / SPP 72 bar / Rotation 60 RPM / WOB 3-10 MT / Torque 5-22 kNm." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1040m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Took SCR's. Performed choke drill." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1050m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Continued drilling cement and float collar at 1050 m MD. Virtually no penetration observed indicating drilling on float collar. Drilling parameters : Flow 3100 lpm / SPP 74 bar / Rotation 60-70 RPM / WOB 7-10 MT / Torque 5-10 kNm." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 3.2 hours. Operational details: Drilled firm cement in shoetrack from 1050 m 1077 m MD. Drilling parameters : Flow 3100 lpm / SPP 76 bar / Rotation 60-70 RPM / WOB 5 MT / Torque 8-12 kNm." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1078m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Broke through 20' casing shoe at 1077 m MD. Observed increased resturn on flowmeter. Picked off bottom and flowchecked - static. Continued drilling to 1078 m MD. Flow 3100 lpm / SPP 77 bar / Rotation 60-70 RPM / WOB 3-5 MT / Torque 4-11 kNm. Meanwhile broke out and laid down adjustable sub setting tool using fwd PRS and fwd IR." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1086m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Cleaned rathole below 20' casing down to 1083 m MD. Drilled new formation from 1083 m to 1086 m MD. Drilling parameters : Flow 3100 lpm / SPP 78 bar / Rotation 70 rpm / WOB 2-4 MT / Torque 4-9 kNm." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1086m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Pumped 40 m3 hi-vis sweep at 3200 lpm to clean well. Meanwhile held toolbox talk prior to displacing to WBM." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.2 hours. Operational details: Displaced well from seawater to 1,20 sg Performadrill WBM with 3500 lpm. Flushed choke and kill lines on BOP and lined up sandtraps." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.8 hours. Operational details: Obtained even MW in/out 1,21 sg." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 0.8 hours. Operational details: Ran in to TD at 1086 m MD. Observed thight spot at 1081-1085 m MD. Spotted 10 m3 LCM pill in rathole. Pulled back into shoe at 1077 m MD." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.2 hours. Operational details: Lined up cement unit. Pressure tested lines prior to performing FIT. Closed BOP. Performed FIT to 1,38 EMW by pressuring up to 21,5 bar on well." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.8 hours. Operational details: Opened BOP and lined up for drilling. Took SCRs. Laid out 5 1/2' singel used for spacing out in shoetrack. RIH to 1077 MD. Obtained MWD pressure point from FIT, EMW 1,408 sg." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1086m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Established drilling parameters : Flow 3000 lpm / SPP 116 bar. Not able to handle flow over shakers. Worked with shaker configuration. Installed coarser top and bottom screens (30/80 mesh)." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1110m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 17 1/2' hole section from 1086 m to 1110 m MD. Drilling parameters : Flow 4000 lpm / SPP 112 bar / Rotation 80 rpm / WOB ~5 MT / Torque 7-8 kNm / ROP 25 m/hrs." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1110m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Lost mud on shakers due to plugged header box and uneven mud distribution. Picked off bottom and reduced flow rate to 1700 lpm to remedy situation. Cleaned shaker box." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1130m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Continued drilling 17 1/2' hole section from 1110 m to 1130 m MD with reduced ROP 10-15 m/hr due to problems to handle fluid returns at shakers. Drilling parameters : Flow 3500-4000 lpm / SPP 103-150 bar / Rotation 120 rpm / WOB 4-7 MT / Torque 3-7 kNm / ECD 1,22. Reamed half stand on connection. Meanwhile repaired shaker #3." "On 2008-05-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1198m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 17 1/2' hole section from 1130 m to 1198 m MD. Drilling parameters : Flow 3500-4000 lpm / SPP 103-150 bar / Rotation 120 rpm / WOB 4-7 MT / Torque 3-7 kNm / ECD 1,22 / ROP 25-35 m/hrs. Reamed half stand on connection. Meanwhile repaired shaker #3." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1240m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Drilled 17 1/2' hole section from 1130 m to 1198 m MD. Drilling parameters : Drilled 17 1/2' hole section from 1130 m to 1198 m MD. Drilling parameters : Flow 3500-4000 lpm / SPP 103-150 bar / Rotation 80-120 rpm / WOB 4-7 MT / Torque 3-7 kNm / ECD 1,22. Meanwhile repaired shaker #3." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1240m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 0.2 hours. Operational details: Reamed full stand due to increaseing ECD 1,22 => 1,25 sg and no sand observed at lag depth for Skade formation. Meanwhile repaired shaker #3." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1240m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Observed massive overflow on lower shaker screens probably caused by sand plugging. Cleaned screens and attempted various flow / screen configurations. Pulled above Skade formation and reciprocated string with 30 RPM and flow rate as dictated by capacity on shakers. Shaker #3 up an running. Dressed all shakers with 145 mesh bottom screens - able to handle flow at 4200 lpm. Cleaned header box." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1302m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued drilling 17 1/2' hole section from 1240 m to 1302 m MD. Drilling parameters : Flow 3800-4200 lpm / SPP 151 bar / Rotation 80-90 rpm / WOB 1-4 MT / Torque 8-12 kNm / ECD 1,25-1,27 / ROP 35-50 m/hrs." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1395m. The activity was categorized as 'drilling -- drill' and lasted for 4.5 hours. Operational details: Drilled 17 1/2' hole section from 1302 m to 1395 m MD. Drilling parameters : Flow 4000-4500 lpm / SPP 136-170 bar / Rotation 80-160 rpm / WOB 3-6 MT / Torque 4-10 kNm / ECD 1,25-1,27 / ROP 35 m/hrs." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1395m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Picked off bottom for flowcheck due to high gas readings ~4% and no loss in active. Flowchecked for 10 min - well static." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1454m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Continued drilling 17 1/2' hole section from 1395 m to 1454 m MD. Drilling parameters : Flow 4500 lpm / SPP ~165 bar / Rotation 160 rpm / WOB ~4 MT / Torque 4-10 kNm / ECD 1,27-1,28 / ROP 50 m/hrs." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1454m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Observed blockage on CRI and conveyer screw. Reduced flowrate and unblocked CRI/conveyer. Estabilshed flowrate and circulated cuttings away from BHA." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1480m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued drilling 17 1/2' section from 1454 m to 1480 m MD at reduced ROP of 20 m/hrs. Experienced shaker screen plugging tendencies / overflow. Drilling parameters : Flow 3500-4100 lpm / SPP 108-147 bar / Rotation 160 rpm / WOB 2-3 MT / Torque 6-8 kNm / ECD 1,27." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1480m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Took SCR's." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1498m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drilling 17 1/2' section from 1480 m to 1498 m MD at reduced ROP of 20 m/hrs. Experienced shaker screen plugging tendencies / overflow. Drilling parameters : Flow 4000 lpm / SPP 142 bar / Rotation 160 rpm / WOB 3-6 MT / Torque 7-10 kNm / ECD 1,28." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1498m. The activity was categorized as 'drilling -- other' and lasted for 1.5 hours. Operational details: Picked of bottom due to problems on shakers. Reciprocated string at 2500 lpm / 60 rpm. Cleaned shaker box. Cleaned shakers and changed to coarser top screens." "On 2008-05-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1568m. The activity was categorized as 'drilling -- drill' and lasted for 3.5 hours. Operational details: Continued drilling 17 1/2' hole section from 1498 m to 1568 m MD. Drilling parameters : Flow 4000 lpm / SPP 142-148 bar / Rotation 160 rpm / WOB ~3 MT / Torque 8-11 kNm / ECD 1,28-1,29 / ROP 25-35 m/hrs." "On 2008-05-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1725m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Drilled 17 1/2' hole section from 1568 m to 1725 m MD. Drilling parameters : Flow 4000-4200 lpm / SPP 142-163 bar / Rotation 160 rpm / WOB 4-6 MT / Torque 12-15 kNm / ECD 1,29-1,30 / ROP 35-40 m/hrs. Meanwhile laid out 5 1/2' HWDP landing string using fwd PRS, fwd IR and foxhole." "On 2008-05-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1782m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 17 1/2' hole section from 1725 m to 1782 m MD. Drilling parameters : Flow 4000-4200 lpm / SPP 142-163 bar / Rotation 160 rpm / WOB 3-5 MT / Torque ~10 kNm / ECD 1,29-1,31 / ROP 40 m/hrs. Started to Increase MW from 1,27 sg to 1,30 sg." "On 2008-05-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1782m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Heard loud bang in drilling module. Picked off bottom and investigated situation. Found that pressure on BOP tensioner cylinders had dropped to 31 bar. Pressurized back to 45 bar. No leaks found." "On 2008-05-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1964m. The activity was categorized as 'drilling -- drill' and lasted for 8.2 hours. Operational details: Continued drilling 17 1/2' hole section from 1782 m to 1964 m MD. Drilling parameters : Flow 4200-4500 lpm / SPP 175-198 bar / Rotation 160 rpm / WOB 4-5 MT / Torque ~11 kNm / ECD 1,31-1,32 / ROP 25-45 m/hrs." "On 2008-05-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1964m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Took SCR's." "On 2008-05-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2129m. The activity was categorized as 'drilling -- drill' and lasted for 6.8 hours. Operational details: Continued drilling 17 1/2' hole section from 1964 m to 2129 m MD. Drilling parameters : Flow 4500 lpm / SPP ~199 bar / Rotation 160 rpm / WOB 4-8 MT / Torque 11-13 kNm / ECD 1,32-1,33 / ROP 40-50 m/hrs. MW in/out 1,30 sg. Initiated steering by dowlinking powerdrive at approx 2105 m MD." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2135m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 17 1/2' hole section from 2129 m to 2135 m MD. Drilling parameters : Flow 4500 lpm / SPP 195-198 bar / Rotation 120-160 rpm / WOB 7-9 MT / Torque 11-15 kNm / ECD 1,31-1,32 / ROP 10-15 m/hrs as determined by geology." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2185m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Observed negative drilling break at 2135 m MD. Observed significant shift in torque and confirmed top of Grid formation on logs. Drilled 17 1/2' hole section from 2135 to 2185 m MD. Drilling parameters : Flow 4500 lpm / SPP 195-198 bar / Rotation 120-160 rpm / WOB 6-8 MT / Torque 18-26 kNm / ECD 1,31-1,32 / ROP 20 m/hrs." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2185m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Got problems with plugged shakers and overflow when Grid sand surfaced. Cleaned shakers and shaker box. Reciprocated string with 500 lpm / 30 rpm. Stepped up rate to 4000 lpm and recommenced drilling." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2209m. The activity was categorized as 'drilling -- drill' and lasted for 2.8 hours. Operational details: Continued drilling 17 1/2' hole section from 2185 m to 2209 m MD with reduced rate as dictated by geology. Drilling parameters : Flow 4400 lpm / SPP ~197 bar / Rotation 120 rpm / WOB 1-3 MT / Torque 6-14 kNm / ECD 1,31-1,32 / ROP 20 m/hrs. Took survey at connection as instructed by DD. Got problems with plugged shakers and had to reduce flow after connection at 2209 m MD." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2239m. The activity was categorized as 'drilling -- drill' and lasted for 4.0 hours. Operational details: Worked on shakers to unplug screens, worked flow rate up and down accordingly. Drilled 17 1/2' hole section from 2209 m to 2239 m MD at reduced ROP ~10 m/hrs. Drilling parameters : Flow 4000 lpm / SPP ~163 bar / Rotation 120 rpm / WOB 5-8 MT / Torque 10-14 kNm / ECD 1,31-1,32. Downlinked powerdrive according to DD's instructions." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2239m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Picked off bottom due to screen plugging on shakers. Cleaned shaker box and screens." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2264m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued drilling 17 1/2' hole section from 2239 m to 2264 m MD at reduced ROP ~10 m/hrs. Drilling parameters : Flow 4000 lpm / SPP ~163 bar / Rotation 120 rpm / WOB 4-9 MT / Torque 11-13 kNm / ECD 1,31-1,32." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2264m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Picked off bottom due to screen plugging on shakers. Cleaned shaker box and screens." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2281m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued drilling 17 1/2' hole section from 2264 m to section TD at 2281 m MD as determined by samples and logs. Top of Balder encountered at 2268 m MD. Drilling parameters : Flow 3800-4000 lpm / SPP 156-168 bar / Rotation 120 rpm / WOB 4-9 MT / Torque 7-12 kNm / ECD 1,31-1,32 / ROP 8-10 m/hrs.." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2240m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Racked back 1 stand. Reciprocated string and circulated hole clean with 3 x bottoms up while stepping up rate from 4000 to 4500 lpm as determined by shaker capacity. SPP 171-207 bar. Rotation 120 rpm." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2281m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: RIH to TD. Sent downlink to set SonicVision in logging mode. Cycled pumps 3 times to obtain correct setting." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2281m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Spotted 10 m3 LCM pill at TD with 1750 lpm as restricted by MWD tools." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2037m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Pulled 5 stand wet. Observed dry pipe." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2037m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well on trip tanks for 15 min - well static." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2037m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Pumped ~8 m3 1,65 sg slug at 1000 lpm / SPP 20 bar." "On 2008-05-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1872m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 2037 m to 1872 m MD. No thight spots observed." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1515m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 17 1/2' drilling BHA on 5 1/2' DP from 1872 m to 1515 m MD. No thight spots observed." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1515m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Gained 350 liters more than theoretical. Performed flowcheck on trip tank - well static." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1064m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: POOH with 17 1/'2' BHA on 5 1/2' DP from 1515 m to 1064 m MD inside 20' shoe. No thight spots observed." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1064m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Performed flowcheck on trip tank - well static." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: POOH with 17 1/2' BHA on 5 1/2' DP from 1064 m to 149 m MD. Performed pit drill with drilling crews - good response from drillfloor." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well on trip tank. Meanwhile performed toolbox talk for removing PS-30 slips." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 110m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Removed PS-30 slips from rotary. Installed master bushing." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 73m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Racked back stand of 5 1/2' HWDP. Broke out 5 1/2' FH x 6 5/8' reg x-over. Broke out and laid out 8 1/4' DC singel. Broke out and racked back stand of 8 1/4' DC." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Broke out and racked back stand of jar and 8 1/4' DC. Broke and laid out NMDC." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 32m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk for laying out Schlumberger drilling BHA's." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Broke out and laid down SonicVison, MWD, ARC and Powerdrive X5." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for retrieving nominal seat protector." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 47m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up jetting sub to stand of 5 1/2' DP. Made up nominal seat protector RT." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH on 5 1/2' DP and latched wearbushing according to Vetco instructions. Picked up and washed/jetted wellhead at 4000 lpm / SPP 60 bar / 3-5 rpm. Made 3 passes across wellhead while circulating." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH with nominal seat protector on 5 1/2' DP from 140 m MD to surface. Broke out RT and jet sub." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for making up pup to cement head." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up cement head and made up 4,5 m 5 1/2' HWDP pup joint. Laid out cement head." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to working on TDS." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 4.8 hours. Operational details: Removed allignment cylinder on TDS. Replaced cylinder with fixed bar and shimms. Parts to hook up bar to brackets missing. Had to produce new parts in mechanic workshop. Meanwhile : -Brought casing running equipment to drillfloor -Drifted 5 1/2' HWDP to 2 3/4' -Removed protectors on 14' casing -Changed head on PDM" "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for dropped object inspection and service on TDS." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Performed dropped object inspection of fwd and aft PRS in manrider." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Made up 2 x-overs and TIW to 14' circulating swedge." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed potential dropped object / tag plates from fwd PRS (finding from dropped object inspection)." "On 2008-05-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.8 hours. Operational details: Worked on TDS. Made up fixed centering bar / brackets on TDS. Meanwhile : -Performed houskeeping and cleaning in shakers -Cleaned pits Static losses to well before midnight ~100 l/hrs." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.0 hours. Operational details: worked on TDS. Made up fixed centering bar / brackets on TDS." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Installed stand in rotary for testing TDS allignment relative to well centre. TDS 5 cm out of centre to STB." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Removed 2 shimmes ea 6 mm from fixed centering bar on TDS. Tested allignement relative to well centre. TDS 9 cm out of centre to port." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.5 hours. Operational details: Reinstalled 2 shimms ea 6 mm and removed 2 ea shimms 1,5 mm. Tested allignment relative to well centre. TDS alligned with well centre but slightly out to port (~1 cm), not able to come closer with availble range of shimms (addtional 0,5-1 mm shimm may be installed at a later point)." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Installed lockwire and secured TDS." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging up 14' casing handling equipment." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Rigged up 14' casing handling equipment. Static losses to well after midnight ~100 l/hrs." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Rigged casing running equipment. Made up LaFleur." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for continued rigging of casing running equipment (new crew)." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Rigged casing running equipment. Installed casing bails." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk for installing FMS and running 14' casing. Lost hydraulics in drilling module due to system trip." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Trip on hydraulic supply to drilling areas due to overheating." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued rigging 14' casing running equipment. Removed master bushing and installed FSM. Functioned slips, tong and elevator. Adjusted backwards travel on casing tong to avoid conflict with elevators. Elevator tilt for BX-2 missing. Rigged up for using tugger to tilt elevator. Meanwhile traced BX-2 elevator tilt adaptor from Sleipner." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Attempted to pick up shoe joint - nogo due to position of eye bolts holding die segments. Sheared eye bolt accidentaly." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: Drilled out / re-threaded eye bolts on elevator and replaced by normal bolts." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to recommencing operation." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Picked up shoe joint and hung off in slips. Picked up and made up intermediate joint, float collar joint and 1st casing joint (#189). Threadlocked couplings. Tested floats in shoe and filled casing." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk with new crew for continued casing running operations and rigging up elevator tilit adapter. Recieved equipment from Sleipner." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 49m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Rigged up elevator tilt adapter for BX-2 frame." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 74m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Recommenced casing running. Not able to latch BX-2 eleavtor onto casing coupling - elevator tillting back when given the closing signal. Troubleshot situation - found no fualts in programming or hook up. Found that elevator needed to have more load for closing. Ran 2 casing joints while troubleshooting." "On 2008-05-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 207m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Ran 14' 96,6# casing from 74 m to 207 m MD. Filled every casing joint with 1,30 sg WBM." "On 2008-05-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 610m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Ran 14' 96,6# casing from 207 m to 610 m MD. Filled every casing joint with 1,30 sg WBM. Static losses approx 100 l/hrs after midnight." "On 2008-05-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 7.0 hours. Operational details: Ran 14' 96,6# casing from 610 m to 1077 m MD. Filled every casing joint with 1,30 WBM. Laid out joint #120 due to jammed protector on box end." "On 2008-05-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1077m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: At 20' shoe, engaged LaFleur onto casing collar. Broke circulation with 100 lpm / SPP 33 bar. staged up pumps to 1100 lpm / SPP 32 bar. MW out 1,30 sg." "On 2008-05-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1540m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Ran 14 96,6# casing from 1077 m to 1540 m MD. Filled every casing joint with 1,30 WBM." "On 2008-05-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1540m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Detected exhaust fumes from gas turbines on drillflloor. Shut down one gas turbine. Moved HTS rollers to pick casing from fwd bay. Meanwhile reciprocated casing." "On 2008-05-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1874m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Ran 14 96,6# casing from 1540 m to 1874 m MD. Filled every casing joint with 1,30 WBM. Laid out joint #48 due to jammed protector on box end." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2126m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Ran 14 96,6# casing from 1874 m to 2126 m MD. Filled every casing joint with 1,30 WBM. Laid out joint #48 due to jammed protector on box end. Joint #14 & #13 added to tally due to lay outs. Meanwhile tested CRI hose to 200 bar. Leakage 3% / 10 min." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up 14' casing pup joint D (4,92 m MD). Took up/down weight 320/276 MT." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Rigged down BX elevator. Broke out and laid down LaFleur tool. Removed casing bails. Installed drilling bails and drilling elevator." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Performed toolbox talk prior to picking up 14' casing hanger / PADPRT." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Picked up and made up 14' casing hanger / PADPRT. Removed rubber protection on PADPRT. Took up/down weight 360/278 MT." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2131m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Removed FMS from rotary." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2134m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Installed master bushing. Checked casing hanger and PADPRT." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2134m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to removing casing tong." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2134m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Rigged down Odfjell casing tong." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2233m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 14' casing / PADPRT on 5 1/2' HWDP from 2134 m to 2233 m MD." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2273m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: On last stand prior to landing casing hanger, broke circulation and staged up pumps : 220 lpm/13 bar, 220 lpm/15 bar, 490 lpm/16 bar. Took 10-12 MT weight at 2243 m MD. Increased flowrate to 1500 lpm / 28 bar. Washed down to 2273 m MD." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2273m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and made up cement head. Hooked up cement hose and controls." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Washed down 14' casing with 550 lpm/18 bar down to 2276 m MD. Landed hanger at 140,84 m MD and set down 7 MT." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Staged up pumps to 2300 lpm / 42 bar. Circulated hole clean piror to cementing. Got a lot of cuttings and cavings over the shakers." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Pumped 20 m3 1,60 sg tuned spacer at 2300 lpm. Lined up cement pump. Dropped 1 3/4' ball for 1st wiper plug. Mixed and pumnped 34,5 m3 1,9 sg cement. Pump rate 500-600 lpm / CUP 15-22 bar. Released dart for 2nd wiper plug and displaced with 2,5 m3 WBM from cement unit. Lined up mud pumps for displacing cement with WBM." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Zeroed stroke counter. Displaced cement with 1,30 sg WBM at 3000 lpm. Bumped wiper plug after 7780 strokes (~97% pump efficiency) by observing 70 bar pressure increase." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Lined over to cement pump and tested 14' casing against float collar / wiper plug to 345 bar / 15 min - ok. Pumped and bled back 2000 litres. No additional flowback observed - floats holding pressure." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set PADPRT in position to set MS seal by applying 30 MT overpull and setting down while rotating 4 times clockwise." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pressure tested surface lines agains kil HCR to 207 bar - ok." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Closed upper pipe rams. Pressurized bulk seal in PADPRT to 207 bar to set MS-seal. Vented DP to athmosphere." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Tested seal assembly to 35 bar / 5 min - ok. Increased pressure to 345 bar - pressure leaked off at approx 3-4 bar / 10 min - trend not improving. Took addtional 10 MT overpull (block 118 MT). Repeated 345 bar test on MS seal with same result. Pumped and bled back approx 400 liter." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Not able to obtain 345 bar test on MS-seal - steady leak off 3-4 bar / 10 min (>1%). Bled off pressure and closed additional valves in kill manifold. Greased valves on cement unit." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Perfomed line test against HCR, 345 bar / 4 bar drop in 10 min. Attempted to re-test MS-seal. Observed volume mismatch and wrong line-up - bled off pressure." "On 2008-05-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Attempted to re-test MS-seal. Pressurized MS seal to 345 bar / 3 bar drop in 10 min but trend not improving. Closed isolation valve on cement unit and monitored pressure on kill manifold from Gesoservice. Pressure Dropped from 329 to 320 bar in 30 min but no improvement observed. Discussed situation. Dedcided to work on valves and lines to obtain better line test before reverting to testing MS-seal." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Greased and operated valves on kill manifold and in moonpool. Changed valve #33 and #35 on cement unit. Greased valves on cement unit. Drained mud from cement unit and filled tanks with water." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pressure tested cement unit against isolation valve. Obtained test to 345 bar with 1,3 bar drop / 10 min." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Tested kill line against valve in moonpool and K3 valve on kill manifold. Pressurized to 35 bar, dropped 0,5 bar / 5 min - ok. Pressurized to 345 bar, dropped 0,7 bar / 5 min - ok. Tested kill line against HCR valves. Pressurized to 35 bar, dropped 0,5 bar / 5 min - ok. Pressurized to 345 bar, dropped 1 bar / 5 min -ok." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up to test MS-seal from above. Pressurized to 35 bar, dropped 0,6 bar 5 min - ok. Pressurized to 345 bar. Pressure dropped 0,7 bar / 5 min in the start but with gradually increasing fall off trend. Dropped 1,8 bar / 5 min towards the end of the test. Pumped and bled back 373 liter. Bled off pressure and discussed situation. Decided to re-attempt pressurizing MS seal with PADPRT tool." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Re-sat PADPRT by applying 30 MT overpull. Pressurized to 207 bar to re-energize MS-seal. Held pressure for 10 min / 1,3 bar drop (0,5%). Slacked off overpull on PADPRT to relax bulk seal. Took 30 MT overpull to expose MS-seal." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up to pressure test MS seal from above. Pressurized to 35 bar, pressure dropped 0,4 bar / 5 min - ok. Pressurized to 345 bar. Pressure dropped at 1,7 bar / 5 min in the beginning but improved towards the end of the test to 0,5 bar / 5 min. Last 10 min 1,1 bar drop (0,32%) - ok. Pumped and bled back 400 liter. Lost 20 MT on block while performing test." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Attempted to released PADPRT by slacking off weight and applying 4 rigihthand turns - nogo. Discussed situation." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Discussed way forward with regards to releasing PADPRT. Repeated PADPRT release procedure but got same negative result." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Awaited instructions for releasing PADPRT." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Reverted to emergency release procedure. Rotated string 13 times counterclockwise until torque bulid up of 10 000 Nm. Attempted to pull free with 40 MT overpull - nogo. Repeated emergency release procedure but got same negative result." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Awaited instructions for releasing PADPRT. Meeting ongoing with town." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2276m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk for attempt to free PADPRT with straight pull release." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Stepped up hookload. Released PADPRT with 60 MT overpull. Observed 30 MT continuos drag after release." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Staged up pumps to 2650 lpm / SPP 25 bar. Circulated riser clean. Got fines over shakers." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Broke out and laid down cement head." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: POOH with PADPRT on 5 1/2' HWDP fdrom 137 m MD to surface. Laid out PADPRT. Found tool cavities packed with cuttings." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to running wearbushing." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up jet sub and testable WBRRT." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 136m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with jet sub / WBRRT on 5 1/2' DP from surface to 140 m MD. Washed across wellhead from 136,5 m to 143 m MD with 2650 lpm." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Set wearbushing at 140,5 m MD according to Vetco instructions. Applied 8 MT overpull to verify setting." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Lined up kill manifold for re-testing MS-seal. Closed UPR. Conducted line test against HCR to 345 bar / 5 min, dropped 0,6 bar - ok." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Attempted to replicate test on MS seal testing against WBRRT. Conducted low pressure test to 35 bar / 5 min - ok. Pressured up to 345 bar, not able to obtain good test, pressure leaked off at approx 3,5 bar / 10 min (~1%) and did not stabilize. Topped up drillpipe and observed for flow up drillpipe. Observed flow from drillpipe. Discussed situation. Decided to pull WBRRT and install test plug for test of MS-seal and BOP." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with WBBRT from 140 m MD to surface. Laid down WBBRT." "On 2008-05-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Made up BOP test plug. RIH with BOP test plug on 5 1/2' DP from surface to 140 m MD." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Set plug in wearbushing according to Vetco instructions. Lined up for testing BOP and MS seal from cement unit." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Pressure tested BOP. Attempted to get test on MS-seal on BOP test #1 against LPR. Pressured up to 345 bar, leaked off at 2 bar / 10 min but did not stabilize." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Pressure tested BOP (test #2)." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.8 hours. Operational details: Pressure tested BOP, test #3 against UPR. Simultaneously pressure tested MS seal to 345 bar. Obtained test result of 1,3 bar / 10 min (0,37%) and improving trend - ok." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 3.2 hours. Operational details: Pressure tested BOP (test #4 to #7)." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.8 hours. Operational details: Pressure tested BOP (test #7 and #8). Reverted to repair on TDS." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- other' and lasted for 5.5 hours. Operational details: Parked TDS for service. Worked on TDS allignment cylinder. Meanwhile pressure tested valves in kill and choke manifolds to 35/345 bar 5/10 min." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Made up test swage to TDS and connected cement hose. Flushed and pressure tested line." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.2 hours. Operational details: Pressure tested upper/lower IBOPs and kelly hose to 35/345 bar 5/10 min - ok." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Rigged down test swage and laid out same." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Continued working on TDS allignment cylinder." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: POOH with BOP test plug on 5 1/2' DP from 140 m MD to surface." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 4.5 hours. Operational details: Continued working on TDS allignment cylinder. Picked up single and installed in rotary for making final allignment on TDS." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up 12 1/4' drilling BHA." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Picked up 12 1/4' powerdrive xceed and hung off in rotrary. Gauged bit. Picked up and made up xceed/motor and made up same." "On 2008-05-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 24m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Picked up C-link assy. Not able to spin in threads. Tendencies of thread gaulling in box. Washed threads. Refurbished and grinded threads as required." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 26m. The activity was categorized as 'drilling -- trip' and lasted for 0.8 hours. Operational details: Reinstalled lift sub on C-link assy to check threads - ok. Made up schlumberger C-link assy - ok." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 61m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Picked up and made up ARC, Powerpulse, Sonicvison, NMDC and NMDC pony. Meanwhile lined up for testing CRI hose and perform injection test. Observed that CRI hose had detached from subsea wellhead. Valve on hose and check valve was dug in the mud/seabed. Attempted to grab valve assembly but could not apply enough force with ROV." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 159m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Made up stand og 8 1/4' DC and jar. Made up stand of DC. Made up x-over. Picked up and made up 4 x 5 1/2' HWDP singles (1 stand). Meanwhile deployed moonpool tugger to assist ROV in recovering CRI valve assembly from mud/seabed." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 159m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Held toolbox talk. Removed masterbushing and installed automatic slips in rotary" "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 526m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 159 m to 526 m MD. Meanwhile worked to recover CRI valve assembly with ROV and tugger assist. Closed valve on subsea wellhead." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 526m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Made up TDS. Circulated according to Schlumberger instructions and performed shallow test of MWD." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2139m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: RIH with 12 1/4' drilling BHA on 5 1/2' DP from 526 m to 2139 m MD. Broke circulation every 500 m." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2139m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Checked allignement of TDS." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2139m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Held handover meeting and toolbox meeting prior to chokedrill. Performed choke drill." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2206m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Continued to RIH with 12 1/4' BHA on 5 1/2' DP from 2139 m to 2206." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2206m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Laid out single from stand #51 to space out for drilling shoetrack and rathole without connection." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2248m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Made up TDS and broke circulation. Whashed down from 2206 m at 2650 lpm / SPP 123 bar and tagged cement plug at 2247,8 m MD." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2248m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Drilled on cement plugs at 2248 m MD. Drilling parameters : Flow 2700 lpm / SPP ~120 bar / String RPM 105 / WOB 3-6 MT / Torque ~5 kNm / ECD 1,31-1,32. Picked off bottom every 10-15 min to clean bit." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2275m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Broke through plugs/float collar. Drilled firm cement from 2248 m to shoe at 2275 m MD. Drilling parameters : Flow 2700 lpm / SPP ~120 bar / String RPM 105 / WOB 1-3 MT / Torque 5-9 kNm / ECD 1,32." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2281m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleaned rathole below 14' casing down to 2281 m MD. Remaed through shoe for every 2 m drilled. Drilling parameters : Flow 2500-3000 lpm / SPP 113-140 bar / String RPM 105-115 / WOB 1-2 MT / Torque ~7 kNm / ECD 1,32." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2284m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Drilled 12 1/4' hole section from 2281 m to 2284 m MD. Drilling parameters : Flow 2500-3000 lpm / SPP 114-145 bar / String RPM 105-115 / WOB 3-4 MT / Torque 7-9 kNm / ECD 1,32." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2268m. The activity was categorized as 'formation evaluation -- circulating conditioning' and lasted for 1.8 hours. Operational details: Circulated at 3000 lpm to clean hole and get even mudweight. Observed clean shakers and even MW in/out of 1,30 sg. Meanwhile made preparations for XLOT. Transferred mud to cementer and flushed kill line to drillfloor. Set choke on cement unit bleed back. Pulled bit inside casing." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2268m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Closed UPR. Verifed line up to standpipe 1 and kill line to BOP." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2268m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 1.0 hours. Operational details: Performed XLOT cycle #1. Pressured up on well to ~100 bar at 92 lpm. observed fall off trend for 15 min. Pumped 1776 l and bled back 775 l." "On 2008-05-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2268m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Performed XLOT cycle #2. Pressured up on well to ~98 bar at 92 lpm. Observed fall off trend for 15 min." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2268m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Bled back after XLOT cycle #2. Pumped 1770 l and bled back 1150 l. Observed pressure bulid up for 15 min after bleed off. Meanwhile had toolbox talk prior to mud displacement." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2284m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 2.8 hours. Operational details: Lined up for mud displacement. Pumped 8 m3 WBM spacer and 10 m3 hv-vis OBM spacer. Tripped in to TD at 2284 m MD. Pumped 200 m3 og 1,30 sg OBM at 3000 lpm / SPP 170 bar. Decreased pump rate to 1000 lpm / SPP 25 bar towards end of displacement. Took WBM back to pits and separated treatable and non-treatable interface." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2268m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 1.2 hours. Operational details: Established closed circulation system. Opened for shakers. Filled poor-boy and sand traps. Filled trip tanks." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2220m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Racked back 1 stand. Picked up single and made up to stand #51." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2280m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: RIH to 2280 m MD and attempted to establish drilling parameters. Pumped at 3000 lpm but got overflow on shakers. Cut back rate to 1700 lpm to be able to handle flow. Stepped up rate to 3000 lpm as dictated by flow on shakers." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2289m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 12 1/4' hole section from 2284 m to 2289 m MD. Drilling parameters : Flow 3500 lpm / SPP 232 bar / String RPM 44 / Bit RPM 144/ WOB 2-3 MT / Torque 7-8 kNm / ECD 1,32 / ROP 20 m/hr. Experienced problems with MWD signal." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2289m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Trouble-shoot MWD signal. Meanwhile drilled ahead 1 m of 12 1/4' hole." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2299m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Drilled 12 1/4' hole section from 2290 m to 2299 m MD. Drilling parameters : Flow 3500 lpm / SPP 232 bar / String RPM 44 / Bit RPM 144 / WOB 2-3 MT / Torque 7-8 kNm / ECD 1,32 / ROP 20 m/hr. Experienced problems with FWD PRS." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2299m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Re-booted software on FWD PRS. Meanwhile circulated with 3000 lpm / 10 rpm and reamed up/down 20 m." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2460m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Drilled 12 1/4' hole section from 2299 m to 2460 m MD. Drilling parameters : Flow 3500 lpm / SPP 232-238 bar / String RPM 120-140 / Bit RPM 220-240 / WOB 3-8 MT / Torque 6-13 kNm / ECD 1,32 / Drilled with limited ROP 20-30 m/hr due to problems with MWD sinal decoding." "On 2008-05-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2591m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled 12 1/4' hole section from 2460 m to 2591 m MD. Drilling parameters : Flow 3500 lpm / SPP 238-249 bar / String RPM 140 / Bit RPM 240 / WOB 3-8 MT / Torque 6-13 kNm / ECD 1,32-1,33 / ROP 30-50 m/hr. Hard stringers encountered at 2518-2519 m and 2565-2568 m MD. Meanwhile inspected CRI hose using ROV." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2593m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Used 4 attempts to downlink to Schlumberger powerdrive. Meanwhile drilled ahead with limited ROP from 2591 m to 2593 m." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2638m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Drilled 12 1/4' hole section from 2593 m to 2638 m MD. Drilling parameters : Flow 3500 lpm / SPP 249 bar / String RPM 140 / Bit RPM 240 / WOB 6-11 MT / Torque 13-18 kNm / ECD 1,32-1,33 / ROP 40-50 m/hr in Ty formation and 10-25 m/hr in Ekofisk formation." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2648m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Used 5 attempts to downlink to Schlumberger powerdrive. Meanwhile drilled ahead with limited ROP from 2638 m to 2648 m. Performed downlink with bit off botm." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2666m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' hole section from 2648 m to 2666 m MD. Drilling parameters : Flow 3500 lpm / SPP 240-246 bar / String RPM 140 / Bit RPM 240 / WOB 11 MT / Torque 14-16 kNm / ECD 1,32 / ROP 10-15 m/hr in Ekofisk formation. Up weight 168 mT / Down weight 150 mT / Rotating weight 157 mT." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2704m. The activity was categorized as 'drilling -- drill' and lasted for 4.2 hours. Operational details: Drilled 12 1/4' hole section from 2666 m to 2704 m MD. Drilling parameters : Flow 3100 lpm / SPP 233-235 bar / String RPM 140 / Bit RPM 240 / WOB 11 MT / Torque 13-14 kNm / ECD 1,32 / ROP 9-10 m/hr in Ekofisk formation. Up weight 171 mT / Down weight 147 mT / Rotating weight 157 mT." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2713m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Used 4 attempts to downlink to Schlumberger powerdrive. Meanwhile drilled ahead with limited ROP from 2704 m to 2713 m." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2754m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Drilled 12 1/4' hole section from 2713 m to 2754 m MD. Drilling parameters : Flow 3500 lpm / SPP 250 bar / String RPM 155 / Bit RPM 255 / WOB 11-12 MT / Torque 19-25 kNm / ECD 1,33-1,34 / ROP 35-40 m/hr" "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2772m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Used several attempts to downlink to Schlumberger powerdrive. Meanwhile drilled ahead with limited ROP from 2754 m to 2772 m." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2788m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Drilled 12 1/4' hole section from 2772 m to 2788 m MD. Drilling parameters : Flow 3200 lpm / SPP 225 bar / String RPM 155 / Bit RPM 255 / WOB 11 MT / Torque 15-35 kNm / ECD 1,33-1,34 / ROP 50 m/hr. Up weight 175 mT / down weight 147 mT / rotating weight 158 mT." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2770m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Performed final downlink and took final survey. RB one std." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2785m. The activity was categorized as 'drilling -- circulating conditioning' and lasted for 5.0 hours. Operational details: Circulated well clean while reciprocated drill string. Pumped 4 x BU at: Flow 3300 lpm / SPP 124 bar / Upwards RPM 40 / Downwards RPM 120. Meanwhile MU and checked gyro tools on main deck. PU and MU gyro tool on drill floor." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2785m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Installed battery and dropped gyro tool string inside DP. Pumped down tool with 500-660 lpm and landed gyro on totco ring at 2659,9 m. Performed rotational shots and gyro tool QC at 2655,9 m." "On 2008-05-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2583m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Flow checked well for 15 min. Ok. POOH 5 stds wet from 2785 m to 2583 m. Flow checked well. Ok. Pumped 5 m3 slug. Meanwhile performed gyro survey on connection while POOH." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2259m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Continued POOH with 12 1/4' BHA from 2583 m and into 14' csg shoe at 2259. Flow checked well for 15 min. Ok. Meanwhile performed gyro survey on connection while POOH." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 133m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: POOH with 12 1/4' BHA from 2259 m to 133 m. Meanwhile performed gyro survey on connection while POOH." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 133m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: BO stand to pick out gyro string. Found gyro tool to be 1 m below connection. MU dedicated fishing tool on tugger and removed tool string out of HWDP. Managed to get gyro data from 2655,9 m to mudline. Meanwhile flow checked well. Ok." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 88m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: RB and LD 12 1/4' BHA from 133 m to 88 m." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- drill' and lasted for 4.8 hours. Operational details: RB and LD 12 1/4' BHA from 88 m to OOH. Cleaned and cleared rig floor." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- other' and lasted for 1.8 hours. Operational details: Held tool box talk with involved personnel. MU and RIH with jet sub and wear bushing retrieving tool from surface to 138 m." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 3.5 hours. Operational details: Jetted area from 138 m to 142 m. Released wear bushing and POOH. LO WBRT assembly and jet sub." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Cleaned and cleared rig floor prior to rigging up for csg equipment." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Serviced TDS and inspected derrick and top drive for loose items after drilling 12 1/4' section." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RU 9 5/8' csg running equipment." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held time out for safety with both crews." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Continue RU 9 5/8' csg running equipment." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held pre job meeting for running csg with focuse on red zone policy. Built scaffolding shelter for csg tong operator on drillfloor." "On 2008-05-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 12m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: PU shoe joint." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 38m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: PU and MU intermediate- and float collar joint. Threads locked connections and checked integrity of shoe and float when RIH." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 49m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with 9 5/8' XO from Vam Top to Vam Top HC. Adjusted roller guides on csg tong." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 272m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: RIH with 9 5/8' Vam Top HC csg w/centr from 49 m to 272 m. Filled csg using top drive every joint. Tripping speed was 6-8 joints/hr. Had hydraulic oil leak on iron roughneck." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 272m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Repaired bursted fitting on iron roughneck." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 339m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 9 5/8' Vam Top HC csg w/centr from 272 m to 339 m. Filled csg using top drive every joint. Tripping speed was 9 joints/hr." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 490m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: RIH with 9 5/8' Vam Top HC csg w/centr from 339 m to 490 m. Filled csg using top drive every joint. Tripping speed was 4-7 joints/hr. Coupling leaking on Odfjell casing tong." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 490m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed leaking coupling on Odfjell csg tong." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 490m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: LO jnt #358 due to damaged box." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1170m. The activity was categorized as 'drilling -- casing' and lasted for 9.5 hours. Operational details: RIH with 9 5/8' Vam Top HC csg from 490 m to 1170 m. Crossed over from Vam Top HC to Vam Top at 753.6 m. Filled csg using top drive every joint. Tripping speed was 6-11 joints/hr." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1170m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held pre-job meeting. Changed to 10 3/4' handling equipment and RU casing circulation tool (FAC). Experienced problems with Odfjell spider elevator." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1170m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Sorted out problem with Odfjell spider elevator." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1188m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: PU and installed XO 9 5/8' x 10 3/4'. Changed out PS21 slips with PS30 slips. Problems with PDM camera." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1188m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired camera on PDM and re-sat HMI software to be able to see picture on the screen." "On 2008-05-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1218m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 10 3/4' csg from 1188 m to 1218 m. Filled csg using FAC tool every joint. Tripping speed was 4 jnts/hr." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1763m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: RIH with 10 3/4' csg from 1218 m to 1763 m. Filled csg using FAC tool every joint. Topped up every 5 joints. Tripping speed was 7-11 jnts/hr." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2640m. The activity was categorized as 'drilling -- casing' and lasted for 9.8 hours. Operational details: RIH with 10 3/4' csg from 1763 m to 2640 m. Filled csg using FAC tool every joint. Topped up every 5 joints. Tripping speed was 5-11 jnts/hr. Broke circulation at shoe with 2200 lpm / 27 bar and circulated 15 min at 1700 lpm / 31 bar." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2640m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Held tool box meeting and RD FAC tool and changed bails. Changed to 5 1/2' HWDP handling equipment." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2640m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: PU and MU 10 3/4' casing hanger / PADPRT assembly. Marked running tool to make sure it was not backing out. Took out master bushing and ran hanger assy through rotary. Re-installed master bushing. Removed csg tong." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2779m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with 10 3/4' x 9 5/8' csg on 5 1/2' HWDP landing string from 2640 to 2779 m MD." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2779m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ball dropped out when PU cement head. Reloaded ball and MU cmt head. Lined up and pressure tested cmt line 345 bar / 5 min." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Established circulation at 1500 lpm / 42 bar and washed down from 2779 m to 2783 m. Landed off 10 3/4' x 9 5/8' csg at 140.5 m and sat down 5 ton. Kept 5 ton on landing string." "On 2008-05-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Circulated casing volume and btms up, a total of 1150 strks, at 1770 lpm / 53 bar loss free rate. Observed 3 m3/hr loss at 2000 lpm but had full return at 1770 lpm." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Continued circulating casing volume and btms up at 1770 lpm / 53 bar loss free rate. Meanwhile held pre-job meeting for cmt job." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Pumped 30 m3 contaminated OBM, 5 m3 base oil and 19 m3 spacer at 1550-1770 lpm / 46-53 bar." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Verified correct line-up by holding and releasing 20 bar through low torque. Mixed and pumped 13,7 m3 1.90 sg cement slurry at 800 lpm / 31 bar." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Pumped 500 ltrs water, released dart and continued pumping 2500 ltrs water behind cement with cmt unit. Top wiper plug sheared at 170 bar. Zeroed stroke counters for mud pumps. Displaced and sheared btm wiper plug by pumping OBM at 1200 lpm using rig pumps. Continued displacing cement with 111.9 m3 OBM at 1770-1500 lpm using mud pumps. Wiper plug sheared at 114 bar / 4450 stks. Slowed down rate to 1000 lpm / 69 bar (FCP) approx 4 m3 prior to bump. Bumped plug with 138 bar after pumping 5080 strokes, which gives a pump efficiency of 96.5%. No losses during displacement." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Equalized pressure with cmt unit and opened lo-torque valve. Pressured up well to 345 bar / 15 min to test casing using cmt unit. Ok. 1250 ltrs pumped and got 1220 ltrs back. Bleed off from 345 bar to 138 bar and checked for back flow to cmt unit. Lined over to rig pumps and bled off from 138 bar to zero on stand pipe. Checked for back flow. Disconnected cmt hoses and flushed lines." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Reduced weight on landing string from 5 mT to neutral and released PADPRT. LD cmt head std. Dropped sponge balls and flushed string using mud. POOH and LD PADPRT." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: PU and RIH with lock down sub from surface to 140 m. Landed lock down sub and made 4 1/4 turns CW, torque 1700 Nm with neutral weight. Toolstring dropped 7.7 inches. Attempted to to set lock down sub. No go." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: 1) Performed line test from cmt unit to HCR valve, 30/220 bar 5/10 min. Ok. 2) Pressured up to set lock down sub against closed top pipe ram. No go. 3) Checked for possible leaks in toolstring by opening IBOP and monitor gain in trip tank. No leak observed. 4) Pressured up to set lock down sub against closed btm pipe ram. No go. 5) Pulled lock down sub 1 m above landing no go. Flushed wellhead with 1100 lpm / 15 min. Landed lock down sub and made 4 1/4 turns CW, torque 1700 Nm with neutral weight. Toolstring dropped 8 inches. Attempted to set lock down sub. No go." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH with lock down sub assembly from 140 m to OOH. Checked lock down sub and verified space out. Ok. LD lock down sub." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: PU and RIH with jet/flush tool from surface to 140 m. Landed out on 140.03 m." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Jetted top of 10 3/4' csg hanger, 750 lpm / 42 bar / 3 rpm / 2 kNm." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: POOH with jet/flush tool from 140 m to OOH. Inspected jetting tool and found indication that tool had not landed out on 10 3/4' csg hanger." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with jet/flush tool from surface to 140 m." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Landed out with jet/flush tool on 10 3/4' csg hanger with 2 mT. PU and established circulation at 910 lpm / 49 bar / 3 rpm / 2 kNm. Tagged with 2 mT serveral times to clean the CH area. PU 1 m and circulated btms up at 930 lpm / 45 bar." "On 2008-05-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 100m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: POOH with jet/flush tool from 139 m to 100 m." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 60m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: POOH with jet/flush tool from 100 m to 60 m. Could not rack back 5 1/2' HWDP due to finger on FWD PRS not working." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- other' and lasted for 3.8 hours. Operational details: Repaired decoder for finger on FWD PRS." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with jet/flush tool from 600 m to OOH. Inspected jetting tool and found indication that tool had not landed out completely on 10 3/4' csg hanger. Decided that it was no point in re-running the jet/wash tool." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 40m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: PU and RIH with lock down sub from surface to 40 m. Could not rack back 5 1/2' HWDP due to finger on fingerboard not working." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 60m. The activity was categorized as 'interruption -- other' and lasted for 7.5 hours. Operational details: Repaired decoder for finger on FWD PRS. Meanwhile changed out drilling bails and performed derrick inspection." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with lock down sub from 40 to 140 m." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Landed lock down sub with 9 mT and made 4 1/4 turns CW, torque 1700 Nm with neutral weight. Toolstring dropped 7.5 inches. Closed UPR and verified correct line-up. Attempted to pressure up to 35 bar without sucess. Switched to second cmt pump and re-tried pumping up to 35 bar. Ok. Continued pressuring up to 207 bar and sat MS seal. Bled off pressure to zero. Confirmed lock by taking 40 mT overpull." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Tested MS in lock down sub 35/345 bar for 5/10 min. Ok" "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Released PADPRT and POOH with running string from 140 m to OOH." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 30m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box meeting prior to running RTTS. MU and RIH with jet sub from surface to 30 m and jetted BOP, 3100 lpm / 22 bar / 10 rpm." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 87m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Continue RIH with jet sub on 4 stds of 5 1/2' HWDP from 30 m to 87 m. PU and MU RTTS w/storm valve. Ran Halliburton centrilizer on single above storm valve." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: RIH with 10 3/4' RTTS w/SSCV on 5 1/2' DP from 87 m to 350 m. Up weight 92 mT / down weight 97 mT." "On 2008-05-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 360m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Reciprocated string and circulated at 290 lpm / 7 bar to clean setting area. Installed RTTS with elements at 350 m and sat down 20 mT, down weight 70 mT." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 350m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Lined up to test RTTS from below. Verified correct line-up from cmt unit to IBOP and performed line test. No go. Closed manual IBOP on TDS and performed line test. Ok. Performed low pressure test to 30 bar / 10 min. Ok. Dropped 1 bar / 10 min. Pressured up in steps and tested RTTS to 230 bar / 10 min from below. Ok. Dropped 1.8 bar / 10 min. 1.3 m3 pumped and 1.35 m3 bled back." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 340m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: PU up to neutral and released from RTTS with 22 turns CCWW. PU to 340 m." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Pulled up and greased top of connection. Ran back down to and spaced out below btm pipe ram." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Lined up cmt unit to IBOP on TDS to test RTTS from above and performed line test to 345 bar. Ok. Performed low pressure test to 30 bar / 10 min. Ok. Dropped 0 bar / 10 min. Pressured up in steps to test RTTS. Pumped 1.1 m3 to 110 bar and observed leak. 500 ltrs bleed back." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Discussed situation and evaluated further action." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Discussed situation and evaluated further action." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Stung back into RTTS. Observed 2.2 bar pressure increase when communication to volume below plug was established. Lined up to test RTTS from below. Closed manual IBOP on TDS. Performed low pressure test to 30 bar / 10 min. Ok. Dropped 0 bar / 10 min. Pressured up in steps and tested RTTS to 230 bar / 10 min from below. Ok. Dropped 1.7 bar / 10 min. 1.33 m3 pumped and 1.32 m3 bled back. Rotated 12 turns to the left and POOH of RTTS. Tested storm valve to 50 bar / 10 min. Ok. Dropped 0.9 bar / 10 min. 121 ltrs pumped and 121 ltrs bled back. Stung out of RTTS." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 348m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Flow checked well prior to displacing well above RTTS to SW. Ok. Meanwhile held tool box talk with involved personnel. Drained trip tank and poor boy degasser. Re-filled trip tank with SW. Displaced well to SW at 3100 lpm / 20 bar. Flushed C & K and surface lines." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 310m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped 10 m3 hi-vis pill at 1500 lpm / 15 bar and spotted above RTTS." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 310m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: POOH with running tool on 5 1/2' DP from 348 m to 310 m. Could not rack back 5 1/2' DP due spinner on iron roughneck not working." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 310m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Investigated problem with pipe spinner on aft roughneck." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 310m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to using chain tong to spin out stds of DP." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 310m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Observed gain in trip tank and flow up RTTS running string. Installed kick valve on string. Shut in well and monitored pressures. No increase in pressure observed. Total gain in trip tank was 420 ltrs." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 292m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Opened auto choke and observed no gain in TT through mud gas separator. Opened kick valve and observed no flow. POOH with running tool on 5 1/2' DP from 310 m to 292 m. Could not rack back 5 1/2' DP due to lower arm on FWD PRS not working." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 292m. The activity was categorized as 'interruption -- other' and lasted for 4.0 hours. Operational details: Changed out solenoid valve on lower arm on FWD PRS. Meanwhile removed every second bolt on slick joint and moved BOP carrier beneath BOP." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 292m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk for manual handling. Performed equipment check and found loose dies on FWD PRS carrier. Changed dies." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: POOH with running tool on 5 1/2' DP from 292 m to OOH." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Cleared rig floor. RIH with 1 single 5 1/2' DP and closed ram. Drained BOP." "On 2008-05-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed diverter pulling tool." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Continued installing diverter pulling tool and POOH with diverter." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: LO diverter." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Continued LO diverter." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: RU for pulling slick joint. Pulled master bushing. Pulled and LO slick joint." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Removed tension cylinders from BOP." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed slings from TDS. PU claxton tool using BX-elevator and ran Claxton tool through rotary. Installed master bushings and 5 1/2' DP slips. Meanwhile unbolted NT2 connector on BOP." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Helt tool box meeting. Moved BOP to stump. MU NT2 connector to stump and adjusted scaffolding according to Vetco request." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.5 hours. Operational details: Held tool box meeting. MU Claxton tool to 5 1/2' DP and installed NT2 connector on to HPDR." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Held tool box meeting before removing tension cylinders. Transfered weight from riser tension system to TDS. PU up to 130 mT. Dismantled tensioner ring system. Meanwhile dismantled annular and cleaned lines from cmt unit through kill, choke and poorboy degasser. Installed cradle and trolly on HTS." "On 2008-05-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Removed moonpool hatch on F-14 and hatch on F-13 for guide wire. Ran 10 mT tugger to moonpool. Production shut down confirmed at 23:55. Meanwhile function tested riser spider." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Slacked off weight from 129 mT to 110 mT to have TBC in neutral. Installed guide wire using 10 mT tugger. Launched hotstab on mini-reel hose down to seabed, attached to guidewire. Removed dummy hot stab and installed hydraulic hot stab into receptacle at top of TBC using ROV." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Operated TBC valve panel to 'Primary unlock' 2-1-1 using ROV and pressured up through mini-reel to 3000 psi. Held pressure for 15 min and confirmed position of indicator rods and unlock band." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 137m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pulled riser 1.5 m above WH using 10-20 mT overpull. Disconnected hot stab and retrieved same." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: POOH with riser until connection for 5 1/2' DP was above rotary. Disconnected 5 1/2' DP from Claxton tool and RB same. MU and RB RT for production riser." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: PU riser and removed master bushings and ring. Positioned split spider and installed same. Meanwhile inspected seal faces in WH and installed debris cover on F-14 using ROV." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pulled HPDR out until first double was above riser spider. Removed fairing on connection using fairing handling tool. Engaged spider dogs and inserted stop bolts. Landed HPDR upper flange on tension joint in riser spider. Removed plastic thread protectors and broke flange connection using Bandak tool." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 109m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Broke flange connection on first double using Bandak tool. LO first double with Claxton tool using main crane and TDS." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 10.8 hours. Operational details: Continued to pull and LO HPDR to deck. Meanwhile brushed and cleaned wellhead using ROV." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box meeting for removing hatch on F-15 and moving riser guide funnel from F-3 to F-14. Removed hatch on F-15." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: RU and ran 6 mT tugger for moving riser landing guide funnel. Hooked on tugger wire to master links on funnel using ROV." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Lifted and moved riser landing guide funnel from F-3 to F-14. Removed debris cap from F-14 and placed on sea bed. Landed and oriented upper guiding skirt on funnel in east direction. Disconnected ROV hooks on master links. Meanwhile removed hatches, built scaffolding/barriers around deck openings and prepared equipment for installing tensioner ring assembly in WH module." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held tool box talk for running production riser with involved personnel." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lifted TBC/stress joint from cantiliver until handling sub was latched into TDS. Unhooked uppermost sling and lifted TBC/stress joint with TDS until it was hanging vertically above rotary. Meanwhile installed VX-ring using ROV, built scaffolding/barriers around deck openings and prepared equipment for installing tensioner ring assembly in WH module." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lowered TBC/stress joint through rotary. Extended riser spider dogs and installed stop bolts in PR holes #3. Hung off stress joint in riser spider. Alligned TBC ROV panels and checked TBC connector for damage." "On 2008-05-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 23m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lifted 1st double with dual lift on block and deckcrane." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 37m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Made up flanged connection according to Vetco/Bandak procedure. Installed fairring on coupling. Ran in and placed TBC connector in level with Weather deck deck. Prepared guidewires in slot F-13 and F-15." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 15m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Placed TBC in in level with Weatherdeck. Function tested TBC according to Vetco instruction. Installed dummy stabs. Oriented lock/unlock panel to 45 deg starboard aft. Attached ROV hooks to guide slings. Hauled guidewires with ROV hooks through Centralizer deck, ran to sealevel. Landed 1 st double in riser spider. Ran guidewires individually to 20 m above seabed." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 66m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed handling tool. Lifted 2nd double to drillfloor with dual lift on block and deck crane. Started MU up flanged connection according to Vetco/Bandak procedure. Meanwhile installed guidewires using ROV." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 118m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 9.0 hours. Operational details: MU up flanged connection on 2nd double according to Vetco/Bandak procedure. Continued removing handling tools, lifting doubles to drillfloor with dual lift on block and deck crane, MU up flanged connections according to Vetco/Bandak procedure and tested flanges to 3000 psi / 5 min, from 66 to 118 m. Could not MU DP due to PRS not operational. Tested deluge system from 10:30 to 10:45 hr." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 118m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired sheared bolts on PRS track on drill floor." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Landed riser on tension joint land off plate in riser spider. MU DP connection to handling sub using TopDrive and manual rig tongs.Lifted PR string and lowered it down to top of riser landing guide funnel (RLGF). Removed hole cover from RLGF and oriented TBC ROV panels. Hook load 97 mT. Continued lowering PR until TBC was 10 cm above VGX gasket." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 6.2 hours. Operational details: Re-arranged lifting slings on RLGF and put tension on wires. Attempted to unlock guide funnel hinge using ROV. No sucess. Fetched crow bar from surface and attempted to bend guide funnel hinge. No sucess. Fetched cutting device from surface and cut guide funnel hinge with tension on RLGF wire slings. RLGF came free. Lowered PR a fraction. Attempted to move RLGF but found that riser weight had landed off on funnel edge. PU PR a fraction and moved landing guide funnel to seabed aft of F-10/F-15. Alligned TBC ROV panel, landed TBC and applied 15 mT. Pumped baseoil to cmt unit and verified line-up to F-12. Performed line test 30 /150 bar 5/10 min against F-12 wing valve. Pumped 8.5 m3 baseoil to pressure up and equalized above DHSV. Opened F-12 DHSV at 93 bar. Displaced cmt unit and kill line to SW." "On 2008-06-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Launched hotstab on mini-reel hose down to seabed, attached to guidewire. Removed dummy hot stab and installed hydraulic hot stab into receptacle at top of TBC using ROV. Production started at 23:25." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Sat TBC ROV panel A in 'primary unlock' 2-1-1 and RIH with PR another 10-15 cm. Sat TBC ROV panel A in 'primary lock' 2-1-2. Sat down 15 mT on PR. Pressured up through TBC port A to 3000 psi and observed silver band alignement of indicator rods above TBC top cap. Silver band was completely aligned. Sat TBC ROV panel A in 'parked position'. Performed 10 mT overpull test to 107 mT to confirmed that TBC was locked. Ok. Sat TBC ROV panel B in 'lower dog flush' x-1-1 and removed dummy hot-stab to be able to observe possible leak." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Lined up to pressure test PR against RTTS plug from cmt unit using SW. Performed line test to 120 bar/5 min. Ok." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Filled riser with SW using cmt unit." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Performed pressure test of PR aginst RTTS plug/14' csg shoe. 20 bar / 10 min 0.6 bar drop 50 bar / 10 min 0.6 bar drop 60 bar / 10 min 0.8 bar drop 70 bar 7 10 min 0.8 bar drop 80 bar / 10 min 0.8 bar drop 90 bar / 10 min 0.9 bar drop 100 bar / 10 min 1.3 bar drop 110 bar / 10 min 4.0 bar drop. 725 ltrs pumped and 560 ltrs bled back. No leak observed by ROV." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pull hot stab out of TBC ROV panel A and insert it into TBC ROV panel B. Flushed upper port on hot stab 'B' with corrosion inhibitor. Meanwhile started to prepare tensioner system in WH module." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Sat TBC ROV panel B in 'upper piston flush' 1-x-x and continued flushing with corrosion inhibitor. Sat TBC ROV panel B in 'parking position' and installed dummy stab. Released and retrieved guide wires for PR. Meanwhile prepared tensioner system in WH module." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 9.5 hours. Operational details: Installed centralizers, boat collision stool and tensioner ring in WH module. Meanwhile lowered PR cutting equipment and valve and equipment for multibowl down to tensioner deck. Changed out encoder on AFT PRS and worked on BOP annular." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held time-out for safety to discuss recent events." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Continued installing tensioner ring in WH module. Meanwhile worked on BOP annular." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Held tool box meeting and RU to install hatches on weather deck. Flushed lines from cmt unit to rig floor with baseoil. Meanwhile closed down production on F-12. Production down at 19:55 hr. Installed hatch on F-13." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Waited on production to confirme valve status. Meanwhile installed hatch on F-15." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Verified line up to F-12. Bled off pressure to choke manifold. Performed line test to 120 bar/5 min." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: Waited for production to verify that DHSV was open and bled off pressure to choke manifold." "On 2008-06-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Continued installing tensioner ring and tension cylinders in WH module. Production up at 22:00 hr. Meanwhile bolted down hatches F-13 and F-15 on weather deck." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Continued installing tension cylinders in WH module. Installed protector guide on tensioner deck. Meanwhile bolted up hatches F-13 and F-15 on weather deck." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Checked level and opened valves on nitrogen system. Transfered weight from TDS to tensioner system. Had 90 bar on all cylinders and 70.5 mT on TDS (neutral) when operation was finished." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Measured cutting hight on PR to 1414 mm above tensioner deck and marked riser. Verified measurement B on machined tectyl coated area. Adjusted weight in TDS to 72,3 mT. RU and leveled cutting tool. Installed auto-feed system." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Started cutting PR production riser using auto-feed and 8-12 rpm." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Completed cutting the PR. Pulled out landing string with top part of Tension Joint. Broke connection between DP and Handling Tool. L/D Top part of Tension Joint." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.5 hours. Operational details: Installed Inflatable Ball inside PR, as a debris barrier for metal swarf during bevelling. Bevelled the PR. Simultaneously worked on the BOP." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Retrieved the cutting gear to the rig floor and rigged down same." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box talk and rigged down the 5½' handling equipment, slings and the Spider. Moved the Spider out from the rig floor." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed outer ring and master bushing and rigged up 5½' handling equipment." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk and broke out the riser RT and LO same." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to install the Multibowl. Had production to shut down the water inject. on F4." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.2 hours. Operational details: M/U the Multibowl and ran in and installed same as per Vetco procedure. Pressure tested to 35 bar to ensure BT seals intack. Energized plastic in upper and lower BT seals, and pressure tested same to 3000 psi (207 bar) 10 min." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Retrieved the Multibowl RT and LO same." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed valves on the Multibowl." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Held time out for safety." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Prepared for running BOP riser jnt. and picked up same. Build scaffolding around the Multibowl." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Ran in and installed the BOP riser jnt. and torqued up same. PU 2.5 tons to ensure locking segment were locked." "On 2008-06-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Retrieved slings for running BOP riser jnt. Installed outer ring and master bushing. Installed hatch cover. Started water injection on F4 at 23:55 hours." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Held tool box talk prior to rig up and change wash pipe. Rigged up for changing out the wash pipe." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Built scaffolding in the Moon Pool to get access to the BOP riser jnt connection. Flushed lines from cmt. to rig floor prior to perform BOP test. Simultaneously worked on the BOP." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 2.0 hours. Operational details: Changed out wash pipe. Meanwhile pressure tested the BOP to 20/345 bars for 5/10 min." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Completed changing of the wash pipe." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.2 hours. Operational details: Rigged up and pressure tested the wash pipe and the IBOP 20/345 bars 5/10 mins. Meanwhile pressure test the BOP to 20/345 bars for 5/10 min." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged down equipment for testing of the wash pipe and IBOP. Installed slings for handling the Diverter. Meanwhile checked torque on bolts on annular." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Lined up and positioned test joint for testing of annular. Tested annular to 20/345 bar 5/10 mins. Meanwhile checked equipment prior to picking up HWDP. Changed dies in flush joint elevators. Held tool box prior to handling of HWDP. Attempted to handle HWDP, not able to open fingers on PDM head." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held tool box talk prior to nippling of the BOP and Diverter. Nippled down the BOP NT2 connector. Meanwhile Changed dies in TDS pipe handler." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Picked up the Diverter and landed on the rig floor. Moved the BOP into to well centre and nippled up same." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled master bushing and ran slick jnt into the BOP." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Held tool box talk and installed the Diverter and made up the NT2 connector." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Cleared and cleaned rig floor." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Held tool box talk and installed hang off wires on TDS." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Prepared handling equipment for slip and cut of drill line." "On 2008-06-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.8 hours. Operational details: Held tool box talk prior to slip and cut drill line." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 1.2 hours. Operational details: Perform slip and cut of drill line." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 3.2 hours. Operational details: Continued slip and cut of drill line." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- maintain' and lasted for 0.5 hours. Operational details: Calibrated top drive." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk prior to install test plug in surface well for testing of BOP riser connection." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.0 hours. Operational details: Made up test plug and RIH and landed off in surface well head." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop activities' and lasted for 1.5 hours. Operational details: Held tool box talk and filled riser to SW and tested BOP connection to 35/345 bars 5/10mins." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: POOH with test plug." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 0.5 hours. Operational details: Held tool box talk and broke out test plug and made up wear bushing RT with Bowl Protector." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: RIH and set Bowl Protector as per Vetco procedure. POOH and laid out Bowl Protector RT." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to handling HWDP." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Checked dies in PRS, PDM and handling equipment prior to pick up HWDP. Unable to handle HWDP with PDM." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Trouble shooted the PDM, found that PDM had to be re-programmed for handling HWDP." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 53m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: RIH with Annulus Insert RT, while picking up dedicated HWDP landing string from cantilever. Found incompatible tool jnts. with 3mm gab." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 53m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: POOH and laid out 3 jnt incompatible tool jnts. Picked up and meassured 3 new jnts." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 113m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Continued RIH with Annulus Insert RT, on dedicated HWDP landing string to 113m." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 139m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up Landing String to TDS. RIH and tagged top of Annulus Insert, with max. 2 ton. Engaged the J-slot and took 1 ton overpull. Slacked off to neutral string weight. Rotated to the left approx 6 turns, while keeping neutral weight to retrieve Annulus Insert." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: POOH and laid out RRT and Annulus Insert. As POOH with the Annulus Insert passed subsea well head very carefully and surface well head wear bushing very slowly due to small clearances." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up Bull nose jet sub and RIH from surface to 140m." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Lined up and washed subsea well reciprocating the pipe, pumped 40m³ SW, 10m³ Hi-vis and displaced riser to 1.03 sg Treated Seawater." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: POOH and L/D Bullnose sub." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up Primary Bowl Protector RRT on DP. RIH and retrieved Bowl Protector, POOH and laid out Bowl Protector." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 1.0 hours. Operational details: Held tool box talk and made up Spear assy. using rig-tongs. Racked back Spear assy. in derrick." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- other' and lasted for 0.2 hours. Operational details: Cleared and cleaned rig floor." "On 2008-06-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk and commenced rig up casing handling equipment and casing tong." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Continued rigging up casing handling equipment and casing tong." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to RIH with 10 3/4' casing." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 108m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Picked up and RIH 10 3/4' Tie-back adapter on 10 3/4' casing from surface to 108m." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up pre-packed 10 3/4' surface casing hanger assembly with Adjustment Sub and casing hanger Handling tool. Made up assembly with low stick-up." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk and released Casing Hanger RT with 10 right hand turns." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Laid out 10 3/4' surface casing hanger handling sub. Changed surface handling equipment to DP." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up premade spear stand from derrick and stabbed into 10 3/4' casing." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk and ran in with 10 3/4' surface casing hanger from 119m to 140m. Tagged subsea tie back well head. Meanwhile drained riser." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Rotated with 3 rpm with torque limit set at 2500 Nm. Observed stall out and Spear released. Engaged Spear again with 12 MT overpull and 2 rpm. Increased torque incrementally in 500 Nm stages. Achieved max torque of 8500 Nm prior to Spear released. Re-engaged with 13 MT overpull and 4 rpm and applied torque. Observed 10,800 Nm make up before spear released." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Took 30 MT overpull, observed 0.5 inch stretch." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released Spear and POOH to surface. Broke off TDS and racked stand back." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk and rigged down Odfjell casing tong." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Broke off and laid out Spear." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk and RIH with one stand of 5½' DP. P/U the 5½' pre-made stand with Adjustment Sub Setting Tool, and made up same." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with Adjustment Sub Setting Tool to 28,6 m. and engaged Adjustment Sub. Applied 140 bar pressure inside tool. Found that tool was engaged in casing coupling just below latch profile, max OP 2 tons. Bled off pressure and lowered tool down approx. 2 cm. Rotated to the right while PU slowly to engage torque slots in adjustment sub. Rotated and landed surface hanger with 11 MT. Took 30 MT overpull. Attempted to release the Adjustment Sub Setting Tool." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Attempted to come up with string and took overpull. Worked string down and rotated 1½ turns. Attempted to pull up and took overpull. Went back down and applied 140 bars to the string, bleed off the pressure and went down, had 10 MT drag going down. Attempted to pull out took overpull immediately. Tool stuck in casing connection just below setting tool latch profile." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Time out involved town organisation." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Set down 20 MT and observed tool came free. Picked up and observed overpull, got tool up into latch profile. Pressure up to 140 bars and took 5 MT overpull. Slacked off weight and bled off pressure simultaneously." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Worked string up and down attempted to free tool. Took 35 MT overpull and worked string up and down. Rotated the string at 10 rpm continuing working string up and down max overpull of 10 MT. Got tool into casing connection again, unable to pull above, but able to move downwards." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 4.0 hours. Operational details: Took out bushing and picked up 10 MT overpull, worked string sideways using tuggers two directions. Able to work string 2 inch's up. Continued working string. Meanwhile discussed options with onshore, decided to go for a straight pull. Performed risk analyses prior to carrying out straight pull to free stuck Adjustment Sub Setting Tool. Drill Quip services hand out of hours." "On 2008-06-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Performed derrick inspection prior to perform straight pull with TDS, to free stuck Adjustment Sub Setting Tool. Serviced TDS." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 6.0 hours. Operational details: Continued derrick-, moon pool- and cantilever inspection prior to performing straight pull with TDS, to free stuck Adjustment Sub Setting Tool. Serviced TDS, FWD and AFT PRS. Laid out DC's and Jars from derrick. Pressure tested FOSV and Gray valve to 30/345 bars 5/10mins." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 5.0 hours. Operational details: Continued with general maintenance on rig floor and in the moon pool. Greased BOP wing valves." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pull stuck Adjustment Sub Setting Tool with straight pull." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Lined up and filled riser with SW. Closed Annular BOP with 1500 psi. Applied pressure on pistons in tool, by pressuring up well (via kill line) in increments of 10 bars to maximum 50 bars. Reduced annulus pressure to 500 psi." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Worked string up and down as per Drill-Quip instructions. Observed string moved up and latching ring engaged setting tool latching profile. Picked up 30 MT overpull. Bled down annulus and opened annular." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Continued working string up and down, picked up overpull in 30 MT increments to max overpull of 150 MT." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Continued working string up and down to max overpull of 150 MT. While options were discussed with land organisation." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Slacked off string weight to neutral and verified string could be torqued up to 9 kNm. Applied 50 bars inside string to verify setting tool integrity." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Prepared surface equipment to pull 10 3/4' Tie back. Checked dies in both PRS's." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to pull 10 3/4' Tie back and surface hanger." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Drained riser. Engaged slot in Adjustment sub with Dril-Quip Tool. Pressured up on HWDP to 140 bars and activated cylinders in tool. Picked up 30 MT to unseat the hanger. Rotated tool 12 turns anti-clockwise to open up the Adjustment sub. Picked up weight to 4 MT over neutral. Rotated tool anti-clockwise with max 2500 Nm torque to back off Tie back connection. Picked up gently on string, with no overpull after 6 turns of rotation. Continued POOH with 10 3/4' Tie back and surface hanger and set in manual slips and made up dog collar." "On 2008-06-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Inspected the 10 3/4' surface hanger, found re-run able. Started manufacturing 'C' plate for handling of 5½' HWDP." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Continued manufacturing 'C' plate for handling of 5½' HWDP. Laid out one DC." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk and SJA prior to run in with 5½' HWDP and brake out top double and lay out same." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Ran in with 5½' HWDP. Picked up and took weight, not possible move up, found Adjustment sub setting tool hung up in casing collar between casing jnt and space out pup. Continued RIH and positioned HWDP collar above 10 3/4' surface hanger." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Serviced broke HWDP collar, picked up HWDP. Installed 'C' plate and 5½' DP elevators on top of 10 3/4' Surface hanger and secured same." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Backed out HWDP double and parked same with AFT PRS." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to change elevators to 10 3/4' casing, changing for longer bails and rig up 10 3/4' casing tong." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Changed elevators to 10 3/4' casing. Changed for longer bails and rigged up 10 3/4' casing tong." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Rigged up 10 3/4' casing tong." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pulled 10 3/4' surface hanger and space out pup up into the rotary table and broke connection. Pulled up the 10 3/4' surface hanger and space out pup with the inner string and surfaced the Adjustment Sub Setting Tool. Inspected the Adjustment Sub Setting Tool and found the engaging ring broken and deformed. Removed the ring." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 4.5 hours. Operational details: Held tool box talk and made up the 10 3/4' surface hanger, ran in same and landed off in RT. Changed to BX4 DP elevator and rigged down the 10 3/4' casing tong. Made up the 5½' HWDP double. Removed the `C` plate and retrieved the 5½' HWDP stand and racked back in derrick. Pulled the Adjustment Sub Setting Tool and laid out same. Retrieved the 5½' HWDP stand below Adjustment Sub Setting Tool and racked back in derrick." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Held tool box talk and rigged up 10 3/4' casing tong and changed to BX3 10 3/4' casing elevators. Pulled the 10 3/4' surface hanger with space out pup." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 103m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk and laid out 10 3/4' surface hanger with space out pup." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Picked up new space out pup and back up 10 3/4' surface hanger and made up same. Ran and landed off in rotary table." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 119m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Changed to 5½' DP BX4 elevator and made up spear assy. Made up spear to HWDP and RIH and engaged the spear in the 10 3/4' casing." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: RIH with surface hanger and tagged Tie back. Rotated the string with 1 rpm and screwed into the Tie back. Torqued up in 500 Nm stages with 13 MT overpull to final torque of 10,500 Nm." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Released the spear and POOH with same. Broke off TDS and racked back spear in derrick." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Rigged down 10 3/4' casing tong." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up 5½' HWDP and XO." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Held tool box talk and picked up the back up Adjustment Sub Setting Tool and made up same to one 5½' HWDP. RIH with the Adjustment Sub Setting Tool and engaged the Adjustment Sub latch profile. Applied 140 bars inside the Setting Tool, compressed Adjustment Sub as per Dril-Quip instruction, rotated totally 14.4 turns. Took 30 MT overpull. Set down string to neutral weight and bled of the pressure, waited for 5 mins for locking dog to relax." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with Adjustment Sub Setting Tool, laid out same and racked back 5½' HWDP in derrick." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up spear assy and broke/laid out same, racked 5½' HWDP in derrick." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk and picked up the HRT with 2 meter DP handling pup. Inspected threads and O-ring seal. RIH with the HRT and made up HRT to the 10 3/4' surface hanger by 10 left hand turns." "On 2008-06-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 140m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Lined up and leak tested the cmt line to rig floor 345 bars 5 mins. Bled of pressure and lined up and leak tested the 10 3/4' Surface tie back casing against the RTTS at 350m, 345 bars 10 mins with SW, volume pumped 409 litres and had 409 in returns." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: POOH with HRT test tool and laid out same." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- casing' and lasted for 3.0 hours. Operational details: Held tool box talk and picked up and RIH with 10 3/4' MS-T seal assy RT. Landed out on 10 3/4' casing hanger. Locked RT into riser. Set seal assy by applying 4300 psi to setting function. Tested seal assy trough test port in multibowl to 345 bar/10 min." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released RT from Casing Hanger and POOH with RT. Laid out same." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 20m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Held tool box talk and picked up and RIH Bowl protector and landed of in surface wellhead. POOH RT, laid out same." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box talk and picked up RTTS pulling tool and made up same as per Halliburton procedure. Started RIH from surface to 10m." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 349m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: RIH with RTTS pulling tool from 10m to 349m." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 349m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Held tool box and displaced well above RTTS plug to 1.30 SG OBM." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 349m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Took up/down weight 81/78 MT. Tagged RTTS plug, screwed into the RTTS with 5 rpm. Pressure increased with 2 bars when equalizing. Picked up 6 MT overpull and released the RTTS plug." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Held tool box talk and POOH with RTTS plug from 349m to surface." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Held tool box and laid out RTTS plug." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: POOH with 4 std of HWDP and jetting sub." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor. Checked dies in PRS." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up 8½' drilling BHA." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 81m. The activity was categorized as 'drilling -- trip' and lasted for 4.2 hours. Operational details: Picked up and made up 8½' drilling BHA and RIH from surface to 81m." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 81m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Laid out jar from derrick and picked up new jar." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- trip' and lasted for 2.5 hours. Operational details: Continued RIH with 8½' drilling BHA, from 81m to 138m" "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- drill' and lasted for 1.5 hours. Operational details: Continued RIH with 8½' drilling BHA on 5' DP, from 138m to 545m. Using the remote operated cleaning and greasing device for the DP. Trip tme 271m/hour." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Tested out the MWD/LWD with 1600 lpm." "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Performed pit drill" "On 2008-06-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Started calibration of Schlumberger MWD block height." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 545m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Contiuned calibration of Schlumberger MWD block height." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 953m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued RIH with 8½' drilling BHA on 5' DP, from 545m to 953m. Using remote operated cleaning and greasing device for the DP. Trip time 326 m/hour." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 953m. The activity was categorized as 'drilling -- drill' and lasted for 0.8 hours. Operational details: Filled the pipe and emptied the trip tank." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1115m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued RIH with 8½' drilling BHA on 5' DP, from 953m to 1115m. Using remote operated cleaning and greasing device for the DP. Trip time 324 m/hour." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1115m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Made up 5' x 5½' XO. and changed over to 5½' surface handlig equipment." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1317m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued RIH with 8½' drilling BHA on 5½' DP, from 1115m to 1317m. Using remote operated cleaning and greasing device for the DP. Trip time 202 m/hour." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1317m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Filled the pipe and emptied the trip tank." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1722m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued RIH with 8½' drilling BHA on 5½' DP, from 1317m to 1722m. Using remote operated cleaning and greasing device for the DP. Trip time 324 m/hour." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1722m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Filled the pipe and emptied the trip tank." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1722m. The activity was categorized as 'drilling -- other' and lasted for 1.0 hours. Operational details: Held choke drill with night and day shift." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1722m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held tool box prior to continue RIH with 8½' drilling BHA on 5½' DP." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2731m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued RIH with 8½' drilling BHA on 5½' DP, from 1722m to 2731m. Using remote operated cleaning and greasing device for the DP. Trip time 403 m/hour." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2754m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Made up to TDS. Washed down and tagged TOC at 2754m. Tagged with 2 MT, Parameters: Flow 1690 lpm / SPP 128 bar / String RPM 50 / TQ 4-6 kNm. MUD weight 1.3 SG." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2758m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Drilled out float from 2754m to 2758m. Drilling parameters: Flow 1690 lpm / SPP 128 bar / String RPM 60 / TQ 5-8 kNm. MUD weight 1.30 SG." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled out shoe track from 2758m to 2783m. Drilling parameters: Flow 1690 lpm / SPP 128 bar / String RPM 60 / TQ 5-8 kNm. MUD weight 1.30 SG. Reamed the shoe and pulled back through shoe with no rotation." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2791m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Drilled new formation from 2788m to 2791m. Cleaned out rate hole and verified no restrictions. Drilling parameters: Flow 1695 lpm / SPP 124 bar / String RPM 70 / WOB 1-5 MT / TQ 6-11 kNm. MUD weight 1.3 SG." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2785m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.8 hours. Operational details: Circulated to even mud weight of 1.30 SG in/out. Meanwhile held tool box talk prior to perform FIT." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Pulled up in the shoe having the bit out of the shoe." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.2 hours. Operational details: Flushed the lines from Cmt unit to the rig floor down the string and up annulus using the Cmt unit. Lined up and leak tested the line from Cmt unit to the rig floor 100 bars. 5 mins. Simultaneously closed the pipe ram of the BOP." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Took FIT equivalent to 1.56 SG, using 1.30 SG heavy OBM. Pumped 70 lpm and applied 71.5 bars to the string and annulus. Shut down the pump. Downhole reading from Schlumberger equivalent to 1,565 SG." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2783m. The activity was categorized as 'formation evaluation -- rft/fit' and lasted for 0.5 hours. Operational details: Pumped down the hole with OBM from the Cmt unit. Lined up for drilling." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2789m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Took survey at 2789m and set tool." "On 2008-06-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2793m. The activity was categorized as 'drilling -- drill' and lasted for 0.5 hours. Operational details: Continued to drill 8½' hole from 2791m to 2793m. Drilling parameters: Flow 1695 lpm / SPP 168 bar / String RPM 100 / WOB 9-10 MT / TQ 10-13 kNm / ROP 8 m/hour / ESD 1.393 SG / MUD weight 1.30 SG." "On 2008-06-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2850m. The activity was categorized as 'drilling -- drill' and lasted for 6.0 hours. Operational details: Continued to drill 8½' hole from 2793m to 2850m. Drilling parameters: Flow 1695 lpm / SPP 163-168 bar / String RPM 100 / WOB 9-12 MT / TQ 5-16 kNm / ROP 8-15 m/hour / ESD 1.391-1.401 SG / MUD weight 1.30 SG. Took survey at 2833m." "On 2008-06-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2932m. The activity was categorized as 'drilling -- drill' and lasted for 10.5 hours. Operational details: Continued drilling 8½' hole from 2850m to 2932m. Drilling parameters: Flow 1985-2080 lpm / SPP 165-180 bar / String RPM 100-160 / WOB 6-9 MT / TQ 7-15 kNm / ROP 8-18 m/hour / ECD 1.44-1.46 SG / MUD weight 1.30-1.35 SG. Took servey at connections. Increased MW from 1.30 SG to 1.35 SG." "On 2008-06-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2930m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took SCR. 1.35 SG OBM at 2930m. 665lpm 31 bars. 890lpm 43 bars." "On 2008-06-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2953m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued drilling 8½' hole from 2932m to 2953m. Drilling parameters: Flow 2050 lpm / SPP 180 bar / String RPM 160-170 / WOB 6-7 MT / TQ 9-14 kNm / ROP 8-15 m/hour / ECD 1.456-1.459 SG / MUD weight 1.35 SG." "On 2008-06-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3012m. The activity was categorized as 'drilling -- drill' and lasted for 5.0 hours. Operational details: Continued to drill 8½' hole from 2953m to 3012m. Reamed Draupne formation as per procedure. Drilling parameters: Flow 2050 lpm / SPP 160-180 bar / String RPM 170 / WOB 2-7 MT / TQ 9-11 kNm / ROP 8-26 m/hour / ECD 1.454-1.456 SG / MUD weight 1.35 SG." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3010m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: As making connection observed gas of 5-7% gas coming back with returns. Circulated down gas to 1 % reciprocating the string, with 1940 lpm, 170 bars, 110 rpm." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- drill' and lasted for 3.8 hours. Operational details: Continued drilling 8½' hole from 3012m to 3070m. Drilling parameters: Flow 1950-2050 lpm / SPP 155-190 bar / String RPM 140-170 / WOB 2-7 MT / TQ 9-12 kNm / ROP 8-32 m/hour / ECD 1.454-1.471 SG / MUD weight 1.35 SG." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3053m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Held pit drill. Took SCR 1.35 SG OBM at 3053m. 443 lpm 23 bars. 665 lpm 34 bars. 886 lpm 47 bars." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3070m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Held tool box talk prior to perform pressure points. Simultaneously circulated well clean while reciprocating the pipe." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3050m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Pulled back one stand, racked back same in derrick and prepared for taking pressure points with stethoscope." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3018m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Made up to TDS, correlated depth and positioned bit at 3018m," "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3032m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Positioned bit at 3032m and down linked twice, activated the Stethoscop." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3057m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: Took pressure point: Bit depth 3031.7m, test depth 3006m, pressure 286.63 bars, mobility 32.53 mD. Bit depth 3042.7m, test depth 3017m, pressure 286.94 bars, mobility 164.08 mD. Bit depth 3056.7m, test depth 3031m, pressure 287.07 bars, mobility 1427.08 mD." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3057m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Down linked and deactivated the Stethoscope. Took survey prior to continue drilling ahead." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3214m. The activity was categorized as 'drilling -- drill' and lasted for 8.5 hours. Operational details: Continued drilling 8½' hole from 3070m to 3214m. Drilling parameters: Flow 1950-2060 lpm / SPP 170-180 bar / String RPM 170 / WOB 4-5 MT / TQ 10-15 kNm / ROP 10-28 m/hour / ECD 1.47-1.48 SG / MUD weight 1.35 SG. Meanwhile rigged up 7' casing tong for making up casing in stands." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3186m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Down linked and deactivated Stethoscop. Reciprocated the string while cleaning prior took pressure point. Bit depth 3185.7m, test depth 3160m, pressure 289.6 bars, mobility 4447.27 mD" "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3141m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Racked back one stand and positioned string. Took pressure point. Bit depth 3140.7m, test depth 3115m, pressure 288.69 bars, mobility 272.88 mD" "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3141m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and deactivated the Stethoscope." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3214m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Washed down to bottom from 3114m to 3214m. Flow 1960 lpm / SPP 175 bar / String RPM 25 / TQ 6-9 kNm / ECD 1.474 SG / MUD weight 1.35 SG. Took survey prior to continue drilling ahead." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3255m. The activity was categorized as 'drilling -- drill' and lasted for 2.5 hours. Operational details: Continued drilling 8½' hole from 3214m to 3255m. Drilling parameters: Flow 1960 lpm / SPP 180 bar / String RPM 160 / WOB 4-6 MT / TQ 12-15 kNm / ROP 8-30 m/hour / ECD 1.474-1.485 SG / MUD weight 1.35 SG. Meanwhile transfered tension cylinders and ring down to the seller deck" "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3255m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Cleaned well prior to take pressure points. Reciprocated the string while cleaning. Parameters: Flow 1960 lpm / SPP 180 bar / String RPM 160 / TQ 9-10 kNm / ECD 1.474 SG / MUD weight 1.35 SG. Racked back one stand." "On 2008-06-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3204m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Positioned string. Started taking pressure point at 3203.7m." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3226m. The activity was categorized as 'drilling -- survey' and lasted for 1.5 hours. Operational details: Continued taking pressure points. Bit depth 3203.7m, test depth 3178m, pressure 289.71 bars, mobility 217.88 mD Bit depth 3225.7m, test depth 3200m, pressure 289.99 bars, mobility 162.61 mD Took survey prior to continue drilling ahead." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3295m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued drilling 8½' hole from 3255m to 3295m. Drilling parameters: Flow 1960 lpm / SPP 175 bar / String RPM 80-160 / WOB 3-6 MT / TQ 10-16 kNm / ROP 8-30 m/hour / ECD 1.465-1.471 SG / MUD weight 1.35 SG." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3295m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Made connection. Took survey prior to continue drilling ahead." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3335m. The activity was categorized as 'drilling -- drill' and lasted for 2.0 hours. Operational details: Continued drilling 8½' hole from 3295m to 3335m. Drilling parameters: Flow 1960 lpm / SPP 175 bar / String RPM 160 / WOB 6-8 MT / TQ 14-15 kNm / ROP 12-22 m/hour / ECD 1.465-1.471 SG / MUD weight 1.35 SG." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3335m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Cleaned well prior to take pressure points. Reciprocated the string while cleaning. Parameters: Flow 2050 lpm / SPP 190 bar / String RPM 160 / TQ 11 kNm / ECD 1.481 SG / MUD weight 1.35 SG." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3335m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Took pressure point: Bit depth 3315.7m, test depth 3290mMD/2839TVD, pressure 291.55 bars, mobility 349.54 mD. Bit depth 3332.7m, test depth 3307mMD/2942,8TVD, pressure 291.83 bars, mobility 55.82 mD." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3335m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Down linked and deactivated the stethoscope. Took survey prior to continue drilling ahead." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3497m. The activity was categorized as 'drilling -- drill' and lasted for 9.5 hours. Operational details: Continued drilling 8½' hole from 3335m to 3497m. Drilling parameters: Flow 2000 lpm / SPP 170-175 bar / String RPM 170-180 / WOB 6-8 MT / TQ 10-16 kNm / ROP 22-27 m/hour / ECD 1.479-1.494 SG / MUD weight 1.35-1.36+ SG. Simultaneously made up 7' casing in stands as a parallel activity and racked back in derrick." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3497m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Down linked and activated the stethoscope, prior to take pressure points. Bit depth 3490.7m, test depth 3465mMD/2993,5TVD, pressure 295.13 bars, mobility 0.1 mD." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3497m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and deactivated the stethoscope. Took survey prior to continue drilling ahead." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3523m. The activity was categorized as 'drilling -- drill' and lasted for 1.8 hours. Operational details: Continued drilling 8½' hole from 3497m to 3523m. Drilling parameters: Flow 2000 lpm / SPP 180 bar / String RPM 180 / WOB 8 MT / TQ 10-17 kNm / ROP 21-26 m/hour / ECD 1.485-1.494 SG / MUD weight 1.35-1.36+ SG. Due to damaged drag chain of the PDM unable to continue make up 7' casing in stands." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3523m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Took flow check due to unexplainable gain. Well stable." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3537m. The activity was categorized as 'drilling -- drill' and lasted for 1.2 hours. Operational details: Continued drilling 8½' hole from 3523m to 3537m. Drilling parameters: Flow 1963 lpm / SPP 185 bar / String RPM 180 / WOB 8 MT / TQ 14-17 kNm / ROP 8,8-26 m/hour / ECD 1.487-1.494 SG / MUD weight 1.35-1.36+ SG. Add primex to reduces to control MW and solids." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3537m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Cleaned well prior to take pressure points. Reciprocated the string while cleaning. Parameters: Flow 1963 lpm / SPP 180 bar / String RPM 180 / TQ 11-13 kNm / ECD 1.466-1,484 SG / MUD weight 1.35+ SG." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3526m. The activity was categorized as 'drilling -- survey' and lasted for 1.0 hours. Operational details: Down linked and activated the stethoscope, prior to take pressure points. Bit depth 3525.7m, test depth 3500mMD/3007,8TVD, pressure 296.21 bars, mobility 5632.91mD." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3537m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and deactivated the stethoscope. Took survey prior to continue drilling ahead." "On 2008-06-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3556m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 8½' hole from 3537m to 3556m. Drilling parameters: Flow 1963 lpm / SPP 170 bar / String RPM 180 / WOB 4-6 MT / TQ 12-19 kNm / ROP 17-26 m/hour / ECD 1.447-1.459 SG / MUD weight 1.35+ SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3577m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 8½' hole from 3556m to 3577m. Drilling parameters: Flow 1963 lpm / SPP 175 bar / String RPM 180 / WOB 4-5 MT / TQ 13-17 kNm / ROP 18-30 m/hour / ECD 1.456-1.463 SG / MUD weight 1.35+ SG. Simultaneously transported flow line Co-flex down to the well head." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3577m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Cleaned well prior to take pressure points. Reciprocated the string while cleaning. Parameters: Flow 1963 lpm / SPP 175 bar / String RPM 180 / TQ 11-13 kNm / ECD 1.449-1,461 SG / MUD weight 1.35+ SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3571m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Down linked and activated the stethoscope, prior to take pressure points. Bit depth 3570.7m, test depth 3545mMD/3029,3TVD, pressure 297.98 bars, mobility 58.39mD." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3571m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and deactivated the stethoscope. Took survey prior to continue drilling ahead." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3617m. The activity was categorized as 'drilling -- drill' and lasted for 2.2 hours. Operational details: Continued drilling 8½' hole from 3577m to 3617m. Drilling parameters: Flow 1963 lpm / SPP 180 bar / String RPM 180 / WOB 5-6 MT / TQ 13-17 kNm / ROP 18-20 m/hour / ECD 1.469-1.471 SG / MUD weight 1.35+ SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3617m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Cleaned well prior to take pressure points. Reciprocated the string while cleaning. Parameters: Flow 1963 lpm / SPP 180 bar / String RPM 180 / TQ 11-14 kNm / ECD 1.461-1,474 SG / MUD weight 1.35+ SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3614m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and activated the stethoscope, prior to take pressure points. Bit depth 3613.7m, test depth 3588mMD/3053,4TVD, pressure 299.86 bars, mobility 38.08mD." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3617m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and deactivated the stethoscope. Took survey prior to continue drilling ahead." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3617m. The activity was categorized as 'drilling -- drill' and lasted for 0.2 hours. Operational details: Made up new stand of DP and prepared for drilling ahead." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3617m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Rig alarm went of and all personnel mustered. Circulated and rotated pipe." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3736m. The activity was categorized as 'drilling -- drill' and lasted for 7.8 hours. Operational details: Continued drilling 8½' hole from 3617m to 3739m. Drilling parameters: Flow 2000 lpm / SPP 180 bar / String RPM 180 / WOB 9-12 MT / TQ 10-20 kNm / ROP 16-26 m/hour / ECD 1.478-1.491 SG / MUD weight 1.35+ SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3699m. The activity was categorized as 'drilling -- survey' and lasted for 0.8 hours. Operational details: Cleaned well prior to take pressure points. Racked back on stand. Parameters: Flow 1600 lpm / SPP 130 bar / String RPM 25 / TQ 11 kNm / ECD 1.447 SG / MUD weight 1.35+ SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3699m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and activated the stethoscope." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3669m. The activity was categorized as 'drilling -- survey' and lasted for 0.5 hours. Operational details: Took pressure point: Bit depth 3668,7m, test depth 3643m MD 3089.58m TVD, pressure 302.52 bars, mobility 16.93 mD." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3669m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked and deactivated the stethoscope. Took survey prior to continue drilling ahead." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3750m. The activity was categorized as 'drilling -- drill' and lasted for 1.0 hours. Operational details: Continued drilling 8½' hole from 3739m to 3750m. Drilling parameters: Flow 1960 lpm / SPP 185 bar / String RPM 180 / WOB 9-13 MT / TQ 14-20 kNm / ROP 9-26 m/hour / ECD 1.475-1.487 SG / MUD weight 1.35+ SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3750m. The activity was categorized as 'drilling -- survey' and lasted for 0.2 hours. Operational details: Down linked Sonic Vision tool in fast record mode." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3750m. The activity was categorized as 'drilling -- other' and lasted for 3.0 hours. Operational details: Circulated well clean 3 time bottom up. Reciprocated the string while cleaning. Parameters: Flow 1960 lpm / SPP 180 bar / String RPM 180 / TQ 12-13 kNm / ECD 1.466-1.473 SG / MUD weight 1.36 SG." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3750m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Flow checked the well stable." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3745m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Took drag and torque reading. 10 rpm = 7.7 kNm, 20 rpm = 7.9 kNm and 30 rpm = 8.6 kNm. Up/down weight 186/145 MT rotation 159 MT, stretch 2.5m." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3536m. The activity was categorized as 'drilling -- trip' and lasted for 1.5 hours. Operational details: Held tool box talk and started POOH with 8½' drilling BHA wet 5 std. from 3750m to 3536m. Held kick drill. Trip time in open hole 142 m/hours" "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3536m. The activity was categorized as 'drilling -- trip' and lasted for 0.5 hours. Operational details: Flow checked well, well stable. Simultaneously made up to TDS and pumped 5m³ 1.56 SG slug." "On 2008-06-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3092m. The activity was categorized as 'drilling -- trip' and lasted for 1.8 hours. Operational details: Continued POOH with 8½' drilling BHA from 3536m to 3092m. Trip time in open hole 253 m/hour." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2689m. The activity was categorized as 'drilling -- trip' and lasted for 1.0 hours. Operational details: Continued POOH with 8½' drilling BHA from 3092m to 2689m into 9 5/8 casing. Trip time in open hole 403 m/hour." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2689m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took flow check. In the 9 5/8' shoe." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2689m. The activity was categorized as 'interruption -- maintain' and lasted for 0.2 hours. Operational details: Function tested BOP. Started service the TDS." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2689m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Took drag and torque reading. 10 rpm = 5.0 kNm, 20 rpm = 5.0 kNm and 30 rpm = 6.0 kNm. Up/down weight 154/135 MT rotation 142 MT, stretch 1.5m." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2689m. The activity was categorized as 'interruption -- maintain' and lasted for 2.2 hours. Operational details: Continued servicing TDS and both PRS's. Meanwhile flushed choke and kill lines." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2m. The activity was categorized as 'drilling -- trip' and lasted for 2.0 hours. Operational details: Continued POOH with 8½' drilling BHA from 2689m to 1919m. Trip time 385 m/hour. Dropped 2 3/4' drift in std # 40." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1116m. The activity was categorized as 'drilling -- trip' and lasted for 2.2 hours. Operational details: Continued POOH with 8½' drilling BHA from 1919m to 1116. Trip time in open hole 357 m/hour." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1116m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Changed to 5' DP handling equipment." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- trip' and lasted for 1.2 hours. Operational details: Continued POOH with 8½' drilling BHA from 1116m to 138m. Trip time 782 m/hour." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 138m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Flow checked well, well static. Simultaneously held tool box talk prior to POOH and lay out 8½' drilling BHA." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 91m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH and racked back HWDP std's." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 91m. The activity was categorized as 'drilling -- other' and lasted for 0.8 hours. Operational details: Removed PS-21 slips and installed master bushing." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 91m. The activity was categorized as 'drilling -- other' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 91m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Installed elevator rotator." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 81m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: Laid out jars." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 62m. The activity was categorized as 'drilling -- trip' and lasted for 0.2 hours. Operational details: POOH and racked back HWDP std." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- trip' and lasted for 3.0 hours. Operational details: POOH and laid out 8½' drilling BHA." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- other' and lasted for 0.2 hours. Operational details: Cleared and cleaned rig floor." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 2.2 hours. Operational details: Held tool box and rigged up 7' liner handling equipment." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Held tool box talk and picked/made up 7' shoe and intermediate." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool/SJA box talk prior to RIH with 7' liner." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 25m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Night shift held BOP drill." "On 2008-06-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 217m. The activity was categorized as 'drilling -- casing' and lasted for 4.2 hours. Operational details: Flow checked 7' float prior. RIH with 7' liner from surface to 217m. Filled first 5 singles, and after every 5'th jnt. Trip time 51m/hour." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 553m. The activity was categorized as 'drilling -- casing' and lasted for 3.8 hours. Operational details: Continued RIH with 7' liner from 217 to 553m. Filled every 5'th jnt. Trip time 90 m/hour. Had unexplainable minor gain." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 553m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Flow checked well, well static." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued RIH with 7' liner from 553 to 600m. Filled every 5'th jnt. Trip time 82 m/hour. Simultaneously continued investigating the leakage. Found Overshot Packer leaking fluid and Koomy unit level dropped." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Held tool/SJA box talk and actuated the Overshot Packer mechanically. Tightened the 16 actuating screws with a max. torque 200 ft-lbs." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 600m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Continued actuating the Overshot Packer mechanically. By tightened the 16 actuating screws with a max. torque 200 ft-lbs." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 708m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: Continued RIH with 7' liner from 600m to 708m. filled every 5'th jnt. Trip time 54 m/hour." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 708m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Flow checked well, well static." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- casing' and lasted for 6.2 hours. Operational details: Continued RIH with 7' liner from 708m to 1068m. filled every 5'th jnt. Trip time 58 m/hour." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to pick up Liner Hanger." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed to 5' DP handling equipment." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- casing' and lasted for 1.5 hours. Operational details: Picked up and installed 7' liner hanger/packer assy according to Weatherford liner hanger procedure. Up/down weight 108/104 MT. Liner weight 36 MT." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed out FMS slips to PS-21 slips." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1068m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed radioactive pip tag blow 7' liner hanger/packer." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Rigged down casing tong." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Picked up and installed Weatherford x-over and pup jnt." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Changed to 5½' DP handling equipment." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Installed two 6m 5½' pup jnt's." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to trip in with 7' line on 5½' DP." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1082m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Checked surface equipment and prepared rig floor for RIH with 7' liner on 5½' DP." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1076m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Laid out one 6m pup jnt." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1294m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: RIH with 7' line on 5½' DP from 1092m to 1294m. Restricted RIH speed when running through Surface and subsea well heads. Trip time 270 m/hour." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2222m. The activity was categorized as 'drilling -- casing' and lasted for 2.8 hours. Operational details: Continued RIH with 7' line on 5½' DP from 1294m to 2222m. Filled every 5'th stand, duration for filling 10-15min. Trip time 338 m/hour. Iron roughneck spinner failed." "On 2008-06-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2222m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Found error in software. Cycled the Iron roughneck and re-booted the software." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2665m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued RIH with 7' line on 5½' DP from 2222m to 2665m. Filled every 5'th stand, duration for filling 10-15min. Trip time 443 m/hour." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2665m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Broke circulation carefully and circulate one liner volume = 21.3 m3, 1300 lpm 48 bars. Took up/down weight 158/140 MT." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3685m. The activity was categorized as 'drilling -- casing' and lasted for 3.5 hours. Operational details: Continued RIH with 7' line on 5½' DP from 2665m to 3685 Filled every 5'th stand, duration for filling 10-15min. Trip time 291/hour. Took weight at 3685m" "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Made up to TDS. Broke circulation and washed down from 3680m to 3700m. 450 lpm 38 bars. Washed through tight spots at 3685m - 3687m and at 3696m. Pressure increased from 38-68 bar at 3700m." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3701m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued washing down from to 3700m. 450 lpm 38 bars. Took 10 mt wt at 3700m. Hole packed off and pump pressure increased from 38 bars to 68 bars." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3694m. The activity was categorized as 'drilling -- casing' and lasted for 2.5 hours. Operational details: Pulled back to 3694m. Circulated well 650 lpm, SPP 40 bars, torque 7-8 kNm. Reciprocated the string during circulation. Evaluated situation with Petek for setting 7' liner shallow to reduce risk and conseqences in continuing working liner to TD.." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3690m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Racked back one double. Installed 6 m pup jnt." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3690m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up and installed Cmt head." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3690m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Held tool box talk prior to space out and circulate." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3690m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Displaced Cmt line to drill water." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3694m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Established circulation at 3694m: 1220 lpm, 73 bars, 10 rpm, up weight 150 MT. Simultaneously held tool box prior to perform Cmt job of 7' liner." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Dropped ball and chased ball with 460 lpm and 22 bars. Ball seated, applied 161 bars to set Weatherford hanger." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Released RT with 8 right hand turn 5 kNm. Slacked of to 100 MT, pressured up to shear out ball seat with 230 bars." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Established circulation: 500 lpm - 27 bars, 1000 lpm - 57 bars, 1500 lpm - 108 bars. Reduced flow to 1000 lpm." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Circulated bottoms up 1490 lpm, 105 bars, 15 rpm and 9-13 kNm torque." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Pumped 5m³ Base oil - 15m³ spacer - 4m³ OBM." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Closed IBOP had 11 bars behind IBOP. Opened the Cmt head low torque valve and re-set flag. Released bottom plug." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Mixed and pumped 22.6m³ cmt. Rotated the string 20 rpm 8-13 kNm. Displaced lines from Cmt unit to Cmt head with 890 litres of fresh water." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Displaced cmt with mud pumps at 1200 LPM. Plug bumped at 2229 stroks. Pressured up to 150 bars and held for 2 min. Pump efficiency 96%." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Bled down to 15 bars on stand pipe manifold. Bled back rest to Cmt unit checked for back flow." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Set packer as per Weatherford instruction. Picked up new pick up weight 150 MT + 4.2 m and slackt of to 100 MT. Observed sheare at 20 MT. Picked up to neutral weight 140 MT." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3695m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Verified line up and pressure tested packer to 310 bars with 1.36 SG OBM. Pumped 1344 litres returns 1305 litres." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Released RT as per Weatherford instructions. Circulated bottoms up 2000 lpm 87 bars. Reduced pump rate due to spacer and cmt at shakers." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Installed two sponge balls in string." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Circulated DP clean up at 2000 lpm 72 bars." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Flow checked well, well static. Simultaneously held tool box talk prior to lay out Cmt head." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Pumped 5m³ slug 1.67 SG." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Cleared and cleaned the rig floor" "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Broke out and laid out the Cmt head with 6 pup." "On 2008-06-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1122m. The activity was categorized as 'drilling -- casing' and lasted for 2.0 hours. Operational details: POOH with 7' line hanger RT 5½' DP from 2616m to 1122m. Trip time 747 m/hour" "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 216m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Continued POOH with 7' line hanger RT 5½' DP from 1122m to 216m. Trip time 906 m/hour" "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 216m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Picked up Cmt head with 6 pup, made up same and broke out the 6 m pup and laid out the Cmt head." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Continued POOH with 7' line hanger RT 5½' DP from 216m to surface. Trip time 432 m/hour." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 10m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Changed out PS-21 slip to master bushing. Cleaned around RT." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Racked back last stand of DP. Broke out 6m pup and laid out the Liner hanger RT." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held tool box talk prior to run with BOP/surface well head cleaning assy." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 72m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up and made up BOP/Surface well head cleaning assy." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 87m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Started cleaning/jetting the BOP/Surface well head with 3100 lpm 70 bars." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 82m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Continued Jet washing the BOP/Surface well head, 3100 lpm, 65 bars. Opened and closed BOP rams." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: POOH with Well protector and washing assy and laid out same." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up one 5½' DP stand ran in and displaced BOP surface lines to water." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Made up wear bushing RT. Ran in and retrieved the Wear bushing after two attempts." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Made up BOP test assy. Ran in and set same." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Lined up for BOP testing. Flushed surface lines." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop activities' and lasted for 4.8 hours. Operational details: Pressure tested the BOP as per Maersk procedure. 20/345 bars 5/10 mins. Simultaneously tested the Rotary hose, auto IBOP and manually IBOP." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Rigged down pressure test equipment and POOH with the test plug." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up Wear bushing RT to one DP stand installed Wear bushing. Made up to TDS." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: RIH with Wear bushing. Washed surface well head, 3700 lpm, 86 bars and 5 rpm. Installed the Wear bushing. POOH with Wear bushing RT." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Lined up for pressure test the well/7' liner against Shear ram." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held tool box talk prior to rig up for RIH with cleaning assy. on 3½' DP. Checked line up to pressure test the well/7' liner." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 1.0 hours. Operational details: Cleared and cleaned rig floor. Started rig up for RIH with cleaning assy. on 3½' DP. Simultaneously pressure tested the well/7' liner to 310 bars 10 min 1.36 SG OBM. Pumped 2375 litres had 2375 litres in return." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Continued rigging up for RIH with cleaning assy. on 3½' DP. Checked out all equipment for loose items. Function tested auto slips. Problems with HTS." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Repaired Power Rollers (HTS)." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up cleaning assy. and made up same as per SPS instructions. PDM could not be operated from dog house." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Electric technician repaired PDM." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Picked up and made up cleaning assy. RIH same on 3 ½' DP from surface to 100m. Picked up 3½' DP singles from cantilever. Trip time 133 m/hour." "On 2008-06-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held tool box talk prior to remove master bushing and install auto slip." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Remove master bushing and installed auto slip." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 600m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 4.5 hours. Operational details: Continued RIH w/cleaning assy. on 3 ½' DP from 100 to 600m. Picked up 3½' DP singles from cantilever. Trip time 111 m/hour. Problems with tail arm of HTS. UP/Down weight at 500m 80/75 MT. Simultaneously started pressure testing of rig manifold." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 630m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Electric technician trouble shooted HTS." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 621m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Troubleshot HTS trailing arm." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 621m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk / shift handover." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 660m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Continued to RIH with cleaning string on 3 1/2' singles from 621 m to 660 m MD. Restriced running speed due to problems with HTS trailing arm / elevator." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 660m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Troubleshot HTS trailing arm and DP elevator. Removed and replaced DP elevator." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1015m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: Continued to RIH with cleaning string on 3 1/2' singles from 660 m to 1015 m MD. Trip speed: 118 m/hrs" "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1015m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to picking up cleaning assemblies #3, #4 and #5. Meanwhile counted 3 1/2' DP joints left on deck." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1022m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Made up 3 1/2' DP pup and cleaning assembly #3 top dress mill. Took up/down weight 90/85 MT." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1022m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Removed automatic slips. Installed master bushing. Found broken safety chain on elevator." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1022m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Removed segment and repaired/welded safety chain on elevator." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1040m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Picked up and made up cleaning assembly #4 top dress mill / well commisioner / well patroller / 9 5/8' razor back and cleaning assembly #5 well sweep magnets." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2073m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: RIH with cleaning assemblies on 5' DP from 1041 m to 2073 m MD. Trip speed: 344 m/hrs" "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2088m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Picked up and made up 5' DP pup and cleaning assembly #6 10 3/4' razor back / posi drift / well sweep magnets / well patroller." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2088m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk for changing to 5 1/2' DP handling equipment." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2088m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Changed elevator insert to 5 1/2'." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2090m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Made up 5' x 5 1/2' x-over." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2090m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Broke circulation. Flow 1100 lpm / SPP 138 bar." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2090m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Changed slips inserts to 5 1/2'. Greased and checked automatic slips. Changed die carriers in iron roughneck." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2590m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.5 hours. Operational details: RIH with cleaning assemblies from 2090 m MD to 2590 m MD on 5 1/2' DP. Trip speed: 333 m/hrs Had to make up TDS while running in due to increased backflow from pipe." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2605m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Scraped and washed FLX packer setting area with 10 3/4' Razor back scraper reciprocating in interval from 500 to 530 m MD. Flow 1850 lpm / SPP 300 bar. Took up/down weights 135/124 MT. Pumped another 50 m3 to condition mud." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2616m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: RIH with cleaning assemblies on 5 1/2' DP from 2605 m to 2695 m MD. Made up TDS. RIH while pumping 500 lpm / SPP 30 bar and passed though liner PBR at 2616 m MD - no obstruction observed." "On 2008-06-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3449m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: RIH with cleaning assembliies on 5 1/2' DP from 2615 m to 2855 m MD. Trip speed: 480 m/hrs" "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3245m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: RIH with cleaning assembliies on 5 1/2' DP from 2855 m to 3245 m MD. Tagged obstruction with ~5 MT WOB at 3245 m MD." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3250m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Made up TDS and broke circulation. Established parameters : Flow 1100 lpm / SPP 130 bar / 20 RPM. RIH and passed thight spot." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3583m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: RIH with cleaning assemblies on 5 1/2' DP from 3250 m to 3583 m MD." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3630m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Made up TDS. Scraped and washed production packer setting area with 9 5/8' Razor back scraper reciprocating in interval from 2575 m to 2605 m MD. Flow 1700 lpm / SPP 300 bar." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3640m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Set torque limit to 16 kNm. Took up/down weights 149/130 MT. Established parameters : Flow 800 lpm / SPP 108 bar / 40 RPM. Free rotating torque 6 kNm. RIH and tagged top of PBR at 2616,6 m MD. Set down 1-2 MT to dress top of PBR. Max torque 8 kNm. Repeated dressing sequence." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3635m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Picked 5 m off bottom and marked pipe for lowest reciprocation depth. Circulated to clean wellbore and condtion mud while reciprocating string. Flow 1760 lpm / SPP 302 bar / 40 rpm." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3635m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Circulated to clean wellbore and condition mud while reciprocating string. Flow 1780 lpm / SPP 297 bar / 40 rpm. Obtained even mudweight in out 1,37 sg." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3640m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Entered PBR at 2616,5 m. Set well commisioner packer by setting down 12 MT." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3640m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Closed UPR. Lined up to pump in kill line. Pressure tested well commisioner packer from above using mudpumps 70 bar / 10 min - ok." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3637m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Bled off pressure through choke and opened UPR. Picked up to neutral weight and unset the well commissioner packer. Pulled back 3 m to 3637 m MD. Found guide for die-holder on drillfloor." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3637m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Prepared for inspection of torque wrench on TDS. Had to abort due to wind speeds above 34 knots. Evaluated situation and decided to continue operations." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3637m. The activity was categorized as 'drilling -- casing' and lasted for 1.2 hours. Operational details: Displaced DP to 25 m3 to base oil. Chased with 4 m3 seawater. Flow 440-1000 lpm / SPP 36-160 bar. Obtained 127 bar static u-tube pressure." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3640m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Set well commissioner packer by setting down 10 MT on liner top. Bled off DP pressure to 4 bar and commenced inflow test of 7' liner." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3640m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Inflow tested liner for 50 min. Pressure increased from 4 to 8,8 bar but levelling out towards the end of the test - ok." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'drilling -- casing' and lasted for 0.2 hours. Operational details: Equalised pressure across packer by applying 125 bar DP pressure. Picked up string 6 m to 3634 m MD to ensure polish mill out of PBR." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Lined up for circulating wash pills. Displaced 11 m3 of dope cleaning pill and 6 m3 Hi-vis pill at 1500 lpm / SPP ~275 bar. Observed leakage on TDS wash pipe." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Stopped displacement. SIDPP 136 bar. Discussed situation and way forward." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Held toolbox talk with relevant personnel." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Bled back dope cleaning pill, Hi-vis and base oil as determined by u-tube pressure. Routed returns back to relevant pits." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3628m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: Racked back stand. Parked TDS and lowered work platform. Changed wash pipe. Inspected die holder on TDS - no parts missing. Meanwhile mixed new well cleaning pills." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Tested TDS/washpipe against IBOP - ok. Picked up stand and RIH to displacement depth. Meanwhile held toolbox talk prior to displacment." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Lined up for circulating wash pills. Pumped ~25 m3 base oil, 10 m3 dope cleaner, 30 m3 1,37 sg Hi-vis push pill, 15 m3 Hi-vis soap pill, 10 m3 seawater and 15 m3 Hi-vis soap pill. Flow ~2000 l / SPP 100-200 bar. Took returns of OBM to pits." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Displaced wash pills with 180 m3 seawater. Stopped pumping and closed annular. Flushed through choke and kill line by pumping addtional 40 m3 seawater. Flow 2200 lpm / SPP ~200 bar. Opened annular." "On 2008-06-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Pumped 1,03 sg packer fluid at 2800 lpm / SPP 297 bar." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Pumped 1,03 sg packed fluid at 2800 lpm / SPP 297 bar. Pumped a total of 222 m3 1,03 sg packer fluid. Measured NTU at end of displacment : 674/527/471/434/386/929/450/365/270." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3634m. The activity was categorized as 'drilling -- casing' and lasted for 1.8 hours. Operational details: Flushed line to cement unit and transferred 1,03 sg packer fluid to cement unit. Positioned tooljoint underneath UPR and closed same. Lined up to test casing/liner through standpipe. Tested production casing/liner to 35/345 bar 5 /10 min - ok. Meanwhile mixed new packer fluid for filling trip tanks." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3622m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Flowchecked visually using flowline camera - well static. Meanwhile mixed new packer fluid - dumped 1 batch due to contaminated water." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3622m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 2.8 hours. Operational details: Mixed new batch of packer fluid in pit#2 - observed percipitate and NTU > 400 when adding Sodium bicarbonate. Suspected contamination from dry additive system (hopper/conveyer). Dumped contaminated packer fluid from pit#2. Prepared for mixing new batch of packer fluid bypassing the dry additive system. Meanwhile serviced and greased TDS." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3622m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Mixed new batch of packer fluid in pit#2. Bypassed dry additive system (hopper) when adding Sodium bicarbonate, got clean fluid." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3622m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to filling trip tanks." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3622m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Lined up and filled trip tanks via standpipe bleed line." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2090m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.8 hours. Operational details: POOH with cleaning assemblies on 5 1/2' DP from 3622 m to 2090 m MD. Checked intervall 3240-3250 m MD for obstruction - none observed. Trip speed: 410 m/hrs" "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2090m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to laying out cleaning assembly #6." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2070m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Broke out and laid down cleaning assembly #6 - 10 3/4' razor back scrapers / posi drift / well sweep magnets / well patroller. Moderate amounts of swarf recovered on magnets, but no large chunks. Changed from 5 1/2' to 5' handing equipment." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1054m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 3.0 hours. Operational details: POOH with cleaning assemblies on 5' DP from 2070 m to 1054 m MD. Trip speed: 346 m/hrs." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1016m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.0 hours. Operational details: Broke and laid out cleaning assembly #5 - well sweep magnets. Assembly #4 - polish mill / well commissioner / 9 5/8' Razor back and assembly #3 - top dress mill was laid out together. Moderate amounts of swarf recovered on magnets, but no large chunks. Changed from 5' to 3 1/2' handling equipment. POOH with cleaning string on 3 1/2' DP from 1054 m to 1016 m MD. Got problems with HTS rollers." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1016m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot problem with HTS rollers." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 230m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 5.0 hours. Operational details: Continued to POOH with cleaning string on 3 1/2' DP from 1016 m to 230 m MD. Laid down 3 1/2' singles. Got problems with HTS tailing arm. Trip speed: 160 m/hrs." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 230m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Troubleshot HTS tailing arm." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 150m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.5 hours. Operational details: Continued to POOH with cleaning string on 3 1/2' DP from 230 m to 150 m MD. Laid down 3 1/2' singles." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 150m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.2 hours. Operational details: Removed PS-21 automatic slips. Installed masterbushing and bowl." "On 2008-06-21, at Well NO 15/9-F-14, a drilling event occurred at a depth of 20m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 0.8 hours. Operational details: Continued to POOH with cleaning string on 3 1/2' DP from 150 m to 20 m MD. Laid down 3 1/2' singles." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- circulating conditioning' and lasted for 1.2 hours. Operational details: Broke out and laid out cleaning assembly #2 - 7' Razor back / well sweep magnets. Laid out cleaning assembly #1 - 6' PDC bit and pup. Small/moderate amounts of swarf recovered on magnets." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: Held toolbox talk for pulling bowl protector. Cleared and tidied drillfloor." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.5 hours. Operational details: RIH with bowl protector pulling tool and jet sub on 5 1/2' stand. Engaged tool at 20,1 m MD according to Vetco instructions. Picked up 0,3 m and circulated to clean wellhead. Flow 3500 lpm / SPP 65 bar. Pumped a total of 10 m3 packer fluid. POOH with bowl protector running tool - no bowl protector recovered." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- casing' and lasted for 0.8 hours. Operational details: Ran back in with bowl protector pulling tool and jet sub on 5 1/2' stand. Broke off TDS. Landed pulling tool at 20,1 m MD. Engaged pulling tool using chain tongs. Made up TDS. Picked up 0,3 m and circulated clean wellhead while picking up slowly. Flow 3500 lpm / SPP 65 bar. Pumped a total of 10 m3 packer fluid. POOH with bowl protector running tool. Broke of bowl protector. Broke out and laid down bowl protector pulling tool." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Made up 5 1/2' FH x 7' VT swadge to stand of 5 1/2' DP and racked back in derrick." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Made up 5 1/2' FH x 7' VT swadge to FOSV's with side entry sub (top of landing stand). Made up top of landing stand to 5 1/2' singel and hung off in aft PRS." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging up tubing running equipment." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Parked IR. Installed and hooked up Odfjell tubing running tong." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Made up tubing hanger landing string comprising of 1 x 12 m 7' tubing, 1 x 6 m 7' tubing, 1 x 1 m 7' tubing, THRT, Swadge with FOSV's and side entry. Used single joint elevator to pick up tubing. Observed damage on pin end of 7' tubing joint in landing string. Observed damage on rig floor tugger wire." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Checked rig floor tugger for damaged and respooled same." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Laid out damaged tubing joint (#240) in landing string. Picked up and made up new 7' tubing joint (#196)." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Made up THRT and racked back TH landing string in derrick. Continued rigging tubing running equipment." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Cleared and tidied drillfloor prior to bringing in control line reels." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk with rig and completion crews." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Spotted WD and BOT control line reels on stb fwd setback. Suspened control line sheave in fwd PRS using PRS lifting tool. Dressed BX elevator with 7' inserts. Dressed slips and dogcollars." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Held toolbox talk with rig and completion crews." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 74m. The activity was categorized as 'completion -- completion string' and lasted for 3.2 hours. Operational details: Picked up of and hung off assy#1 Ratcheting muleshoe / stinger. Picked up and made up assy#2 - 9 5/8' Granite packer. Picked up and made up assy#3- 20' completion PBR. Made up and ran 3 x 7' tubing joint." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 88m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Picked up and made up assy#4 DHPG/CIV. Made up joint on top of completion assy#4 to ease termination of controlines." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 88m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to terminating DHPG/CIV completion assemblies." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 88m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Stripped and splitted control line. Terminated DHPG cable according to WD procedure. Tested conductivity - ok. Tested cable fitting to 10.000 psi through test port - ok." "On 2008-06-22, at Well NO 15/9-F-14, a drilling event occurred at a depth of 88m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: RIH with tubing to place in working height for terminatining CIV control line. Stripped and bevelled control line. Installed CIV in carrier. Tested control line termination fitting to 10.000 psi through test port - ok. Tried to obtain ~50 bar on control line, hydraulic pump not suited for supplying low pressure (spiked when pressuring up). Pressure up several time to obtain stable pressue. Hard to determine if there was a leakage on fitting closest to the carrier." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 88m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Cleaned and air blasted check valve assembly and fittings to check for leaks. Observed no leaks - control line pressure steady on 25 bar - ok." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Made up 7' tubing joint (#234). High and erratic thread torque. Backed out connection, cleaned threads and observed gaulling. Laid out joint #234. Refreshed box on joint #235. Picked up and made up next tubing joint - ok." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 100m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Removed masterbushing. Installed and hooked up FMS. Had problems with HTS tailing arm." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 100m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Troublehshot HTS tailing arm." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 100 m to 240 MD. Installed control line clamp/protector on every collar." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 240 m to 300 m MD. Installed control line clamp/protector on every collar." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 300m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Held toolbox/handover meeting. Checked and greased equipment." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 785m. The activity was categorized as 'completion -- completion string' and lasted for 9.0 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 300 m to 785 m MD. Installed control line clamp/protector on every collar. Average running speed 54 m/hrs." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 842m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 785 m to 842 m MD. Installed control line clamp/protector on every collar. Tested combination of tubing tong die inserts with regards to marks/damage on tubing. Decided to run with standard die inserts below GLV. Average running speed 13 m /hrs (due to die trials)," "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1081m. The activity was categorized as 'completion -- completion string' and lasted for 4.0 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 842 m to 1081 m MD. Installed control line clamp/protector on every collar. Average running speed 60 m/hrs." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1081m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot HTS tailing arm." "On 2008-06-23, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1177m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 1081 m to 1177 m MD. Installed control line clamp/protector on every collar. Average running speed 77 m/hrs." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1249m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 1177 m to 1249 m MD. Installed control line clamp/protector on every collar. Average running speed 72 m/hrs." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1269m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: Picked up and made up assy#4 Schlumberger gas lift mandrel. Counted joints left on deck - 138 - ok. Removed FMS and installed masterbushing for using manual slips. Made up tubing joint on top og assy#4 to ease bypassing with control line. Stripped control line mantle. Installed clamps and inserts across GLV slot. Installed extra clamp on #assy4 upper pup joint due to bend on controll line. Removed masterbushing and installed FMS. Dressed tong with low marking dies." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1400m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 1269 m to 1400 m MD. Installed control line clamp/protector on every collar. Got problems with HTS conveyer belt. Average running speed 75 m/hrs." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1394m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Troubleshot problem with conveyer belt. Meanwhile greased slips and elevator." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1400m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Troubleshot HTS. Found burned power distribution circuit. Made repair as required." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1565m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 1400 m to 1565 m MD. Installed control line clamp/protector on every collar. Average running speed 73 m/hrs. Observed leakage from BX elevator." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1565m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Changed damaged hose on BX-elevator." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1732m. The activity was categorized as 'completion -- completion string' and lasted for 3.0 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 1565 m to 1732 m MD. Installed control line clamp/protector on every collar. Average running speed 55 m/hrs." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1851m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 1732 m to 1851 m MD. Installed control line clamp/protector on every collar. Reduced running speed due to increasig drag ~5 MT in well when completion assemblies enetered 9 5/8' casing. Average running speed 43 m/hrs." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2100m. The activity was categorized as 'completion -- completion string' and lasted for 3.8 hours. Operational details: Ran 7' 29# S13%Cr110 tubing from 1851 m to 2100 m MD. Installed control line clamp/protector on every collar. Average running speed 66 m/hrs." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2100m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to lifting in assy#6 FLX/ASV. Counted joints left on deck - 67 - ok." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2100m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Removed FMS and installed masterbushing. Lifted assy#6 FLX/ASV onto HTS. Lifted in assy#6 with elevator and drillfloor tugger and made up same." "On 2008-06-24, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2100m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Took measurements. Cut, stripped and splitted control line. Dressed DHPG control line ends. Installed and made up splice cylinder according to WD procedure. Installed lower connector on chemical injection line." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2100m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Tested fittings on DHPG lower spilce fitting through dedicated test port 10 min / 10000 psi - ok. Got problem with chart recorder. Continued testing by visual observation. Tested upper DHPG splice fitting 10 min / 10000 psi - ok." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2100m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Tested fitting on chemical injection line lower connector 10 min / 10000 psi - ok. Installed upper conncetor on chemical injection line. Mated chemical injection line connectors. Tested upper fitting on chemical injection line 10 min / 10000 psi - ok. Meanwhile lowered sheave suspended in PRS due to hydraulic leak from PRS." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2100m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Installed connector protection clamp and adjusted same. Picked up and took in slack on control line by adjusting standard clamp below. Rigged up sheave for DHSV/ASV control line. Blinded off redundant hydraulic line from FLX/ASV and secured same in connector protection clamp. Ran FLX/ASV through RT and checked same according to BOT procedure." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2108m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Made up 7' tubing joint to assy#6. Cut and dressed control lines for splicing." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2108m. The activity was categorized as 'completion -- completion string' and lasted for 2.8 hours. Operational details: Dressed dual control line for ASV/DHSV and fed through sheave. Made up ASV control line according to BOT procedure. Tested ASV control line to 570 bar / 10 min - ok. Tested redundant control line to 345 bar / 10 min - ok. Installed blind fitting on redundant line." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2108m. The activity was categorized as 'completion -- completion string' and lasted for 2.2 hours. Operational details: Flushed chemcial injection line and confirmed correct line up. Installed chemical injection lower connector and tested fitting to 10000 psi / 10 min - ok." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2108m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Spliced DHPG control line above FLX/ASV according to WD procedure. Tested conductivity - ok." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2108m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Pressure tested uppr/lower fitting on DHPG splice to 10000 psi / 10 min -ok. Connected chemical injection line and tested fitting on upper connector to 10000 psi / 10 min - ok." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2108m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Installed protectors/clamps and adjusted to take slack on control lines." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2108m. The activity was categorized as 'completion -- completion string' and lasted for 0.2 hours. Operational details: Function tested ASV according to BOT procedure - ok." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2018m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Picked and made up assy#7 DHSV. Picked up 7' joint (#62) and made up same to ease installation of control line and protectors/clamps." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2130m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Installed and fitted control line special clamps accross DHSV. Flushed DHSV control line and made up same to DHSV according to BOT procedure. Tested DHSV contrrol line to 570 bar / 10 min - ok." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2156m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Removed master bushing and installed FMS in rotary. Ran 1 joint of tubing." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2156m. The activity was categorized as 'completion -- completion string' and lasted for 0.5 hours. Operational details: Perfomed toolbox talk / handover meeting (new Mærsk drilling crew)." "On 2008-06-25, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2498m. The activity was categorized as 'completion -- completion string' and lasted for 4.5 hours. Operational details: Ran 7' 29# S13%cr110 tubing from 2156 m MD to 2498 m MD. Installed control line clamp/protector on every collar. Average running speed 76 m/hrs." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Ran 7' 29# S13%cr110 tubing from 2498 m MD to 2596 m MD. Installed control line clamp/protector on every collar. Average running speed 65 m/hrs." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: Changed insert in BX elevator to 5 1/2'. Counted joints on deck - 27 - ok. Picked up landing stand with 7' swadge. Installed control line clamp. Made up landing stand to completion string. Made up TDS. RIH with completion on 5 1/2' landing stand. Started pumping at 200 lpm when passing 2610 m MD. Tagged with ~5 MT at 2615,4 m MD without observing pressure build up. Picked up ~2 m to index ratcheting muleshoe and tried to enter PBR twice more - nogo. Picked up 3-4 m, ran in and entered PBR on 4th attempt. Observed pressure bulid up and reduced fluid returns when entering PBR, shut down pump. Tagged top of PBR with end of string at 2620 m MD." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Pulled out with landing stand. Broke out landing stand and racked back same. Changed inserts in BX elvevator to 7'. Meanwhile performed space out calculation." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- completion string' and lasted for 1.2 hours. Operational details: Laid out joint #16 and replaced with joint #21 to put stinger no-go 0,35 m above PBR. Prepared for picking up tubing hanger." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Picked up and made up 13 5/8' TH with handling tool. Cut, stripped and prepared control lines for pulling through TH." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Installed fittings on control lines and pulled control lines through TH. Made up fittings on control lines on bottom/top of TH. Unable to get good test on TH penetration fittings." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'interruption -- repair' and lasted for 5.5 hours. Operational details: Found leakage across fittings for DHSV. Made several attempts to fix fitting with locktite - negative. Took out DHSV control line. Removed fittings and installed new ones. Applied lock tite to fitting threads." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Allowed locktite thread compound to harden prior to pressure test." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pressure tested TH fittings to 35 / 345 bar 5 / 10 min - ok." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed C-plate. Landed TH in C-plate." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Broke off TH handling tool and laid down same." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Wrapped control lines around tubing hanger neck. Installed communication collar and teminated 3 ea hydraulic lines in same. Changed to 5 1/2' inserts in BX elevator." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2596m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Picked up TH landing stand. Made up THRT to TH with 9 counterclockwise turns using chain tongs. Made up control lines for chemical injection, ASV and DHSV to THRT. Pressure tested DHSV/ASV control lines. Made up control lines for THRT activation." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2613m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Removed C-plate and masterbushing. Ran TH/THRT through rotary. Installed masterbushing. Positioned stinger at 2613 m MD approx 3 m above PBR at 2615,4 m. Made up cement hose to side entry on landing string. Marked tubing with TH landing point." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2613m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Lined up for pumping baseoil down tubing taking returns to pits. Checked out alarm on mud pump liner spray." "On 2008-06-26, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2613m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Pumped baseoil in to tubing at 200 lpm to obtain underbalance in well." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2613m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pumped baseoil in to tubing at 200 lpm to obtain underbalance in well. Pressure increased from 0,5 bar to 6,9 bar during displacement. Pumped a total of 10 m3. Took up/down weight 170/150 MT." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2613m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Ran in and attempted to land TH in wellhead. Unable to enter PBR at 2615,4 m MD. Picked up and attempted several (12) times to enter PBR - negative. Set down max 7 MT. At last attempt, observed that string moved incrementallly (2-3 cm) for each time weight was set down. Discussed situation - meanwhile maintained ~5 MT downweight. Observed sudden drop in applied weight - stinger free to move downwards. Drained riser. Landed tubing hanger at correct datum mark. Observed pressure buliding up from 6 bar to 11 bar indicating sealstem travel." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Tested tubing hanger through port#1 and #2 in multibowl, 35 bar / 5 min - ok. Pressured up TH function line to enagage tubing hanger lock ring. Performed overpull test to 185 MT, i.e. 15 MT above last upweight. Lined up cement unit and performed line test against closed lo-torque valve on landing stand, 345 bar / 5 min - ok." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Pressure tested tubing/sealstem to 50 bar / 5 min - ok. Volume pumped 149 liter." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.2 hours. Operational details: Closed DHSV and bled off pressure above to ~3 bar. Bled back 30 liter. Held inflow test for 10 min - ok. Equalized across DHSV and opened same. Volume pumped 50 liter." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.8 hours. Operational details: Pressured up to 345 bar at 120 lpm to set production packer and test tubing. Held test for 25 min - improving trend last 15 min (5 min 1,3 bar => 5 min 0,7 bar => 5 min 0,5 bar) - ok. Pumped a total of 1088 liter. Packer installed at 2598 mMDRT." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Bled down tubing pressure to 280 bar, bled back volume 180 liter. Closed DHSV and bled off pressure above to 156 bar, bled back volume 90 liter. Not able to adjust the choke to the intended 210 bar. Inflow tested DHSV to 125 bar differential. Held test for 15 min - increased 0,2 bar last 5 min with improving trend - ok." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Bled down tubing pressure from 156 bar to 10 bar to put 270 bar differential across the DHSV. Bled back 100 liter. Held inflow test for 30 min - test improving by time, last 5 min 0,02 bar increase. Equalised pressure (280 bar) accross DHSV and opened same. Pumped 190 liter. Bled back pressure on tubing to line up for pressure testing annulus. Total bled back volume 940 liter." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3620m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.0 hours. Operational details: Lined up to maintain pressure on string while pressuring up tubng x casing annulus. Rigged down kill hose from F-12 and attached to hose on F-14 A-annulus. Pressured up to 100 bar on tubing." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Lined up cement unit and performed line test against closed lo-torque on A-annulus, 35/345 bar 5/10 min - ok." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.2 hours. Operational details: Pressured up to 330 bar on A-annulus to set FLX packer and test production packer from above. maintained pressrue on tubing >100 bar. Held pressure for 15 min / 0,2 bar drop - ok. Total volume pumped 1107 liter. Vented B-annulus while performing test." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.5 hours. Operational details: Bled down pressure on A-annulus to 270 bar, bled back 60 liters. Closed ASV and bled off pressure above to 200 bar to put 70 bar differential across ASV, bled back 160 liters. Inflow tested ASV for 15 mins - ok." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 0.8 hours. Operational details: Bled down pressure above ASV to 10 bar to put 260 bar differential across ASV, bled back 160 liters. Maintained ~90 bar in tubing. Inflow tested ASV for 30 mins - ok." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2620m. The activity was categorized as 'completion -- test scsssv' and lasted for 1.2 hours. Operational details: Equlized accross ASV by pressuring up on A-annulus to 270 bar, pumped 220 liters. Bled off annulus pressure to zero. Bled off pressure on tubing from 90 bar to zero." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Disconnected cement hose from cement manifold. Released THRT by 9 clokwise turn and picked up 1 m. Secured cement hose on landing string." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 0.8 hours. Operational details: Displaced landing string and riser to seawater pumping 15 m3 at 2000 lpm. Rigged down cement line. POOH with THRT and detached control lines from same." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.5 hours. Operational details: Broke THRT from landing string. Broke landing string and laid down 2 x pup and 1 full joint." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 2.0 hours. Operational details: Rig down and removed tubing running equipment, sheaves and reels from drillfloor." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.0 hours. Operational details: Made up BPV setting tool. RIH with BPV and set same at 20,4 m MD according to Vetco instructions. POOH with BPV setting tool and laid down same." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- completion string' and lasted for 1.8 hours. Operational details: RIH with 5 1/2' DP stand to 19,5 m MD. Attached air hose fitting to 1502 hub on standpipe. Displaced riser to air." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held handover meeitng / toolbox prior to nippling down diverter, BOP and riser." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Laid out tubing single and 2 x pups form landing string. Undid nuts on slick joint." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Removed master bushing and outer ring from rotary." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Changed to 5' inserts in elevator to accommodate conductor housing pulling tool. Released mechanical seals on overshot." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed 10' split inserts in diverter. Picked up diverter release tool. Not able to engage and release diverter." "On 2008-06-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Attempted several times to engage and release diverter - negative. Laid down diverter release tool." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed elevator and attached slings to bails. Pulled diverter using slings and set back same." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Pulled overshot joint using slings. Installed outer ring and masterbushing." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Dismanteled BOP tension cylinder and pulled aside. Racked back overshot joint. Cleared drillfloor for pulling BOP riser joint." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Disconnected NT-2 on BOP. Installed cradle in HTS. Installed slings for pulling riser BOP riser joint." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Skidded BOP to stb storage. Attached 2 ea 10 MT slings to BOP riser joint padeyes." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Disconnected BOP riser joint NT-2 on wellhead. Removed scaffolding on weather deck." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed scaffloding on weather deck. Removed split hatches in weather deck. Removed masterbushing. Confirmed well F-4 shut in with no pressure. Picked up riser and drained out seawater inside." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pulling riser." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Pulled BOP riser through wellhead moudule, moonpool and rotary. Laid out riser on HTS cradle." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'drilling -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Installed and secured hatch on weather deck. Installed dart in BPV." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Removed communication collar and unwrapped control lines as required. Fitted graphoil seals and fed control lines through dedicated ports in wellhead. Made up external fittings on control lines to energize graphoil seals. Installed VG137 seal on multibowl and VG63 seal on top of tubing hanger. Filled void with hydraulic oil. Meanwhile cleaned and tidied wellhead and prepared for lifting down XMT spool." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 4.0 hours. Operational details: Transferred and installed XMT spool on wellhead according to Vetco instructions. Made up NT-2 connector. Energized BT seal pumping plastic sealant through port #7/#8 (up to 5000 psi). Tested VG63 seal by applying 500 psi through port #9/#10. Tested TH void through test port #5/#6 to 345 bar / 15 min - ok. Meanwhile attached slings onto TDS bails for lifting XMT." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Picked up XMT with port overhead crane in moonpool and landed XMT on Weatherdeck. Transferred XMT to slings from drillfloor. Backed up lift sideways using 6 T moonpool tugger." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed F-9 hatch and beam for passing through XMT." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Lifted XMT though weather deck and placed onto spool pice on XMT deck. Orientated tree according to instructions from Vecto/production dept. Made up Graylock connection." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Installed hatches on weatherdeck. Pressure tested seal ring between spool and XMT to 35 bar / 10 min through test ports #3 and #4. Installed teflon seal rings and made up exit blocks for hydraulic lines." "On 2008-06-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed exit block for DHPG control ine. Had problems with broken allen bolt, installed new bolt. Tested exit block to 10000 psi according to WD procedure - not able to get good test. Discussed situation - test in SH procedure specified 5000 psi test. Re-tested exit block to 5000 psi, but still not able to get good test. Broke off exit block and removed excess paint from WH and exit block. Polished exit block seal surface. Installed exit block, hooked up Vetco pump with recorder and tested exit block to 500/5000 psi 5/10 min -ok. Meanwhile pulled and laid down diverter." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Spliced DHPG cable. Made up DHPG wellhead outlet to exit block according to WD procedure. Pressure tested wellhead outlet - negative. Observed leakage around threads between wellhead outlet and exit block. Dismanteled wellhead outlet and found damage on primary metal seal around threads. Discussed situation. Decided to go ahead with XMT hook up activities. Meanwhile serviced TDS." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Installed flow spool on XMT with tugger support from drillfloor according to instructions from production." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Made up XMT flow spool with hy-torq kit. Worked to hook up coflex hose to wellhead module production hub. Used slings, chainhoists and eagle clamps as required to support/jack coflex hose. Meanwhile hung off travelling block for 6 month maintenance of crown block." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.5 hours. Operational details: Hooked up coflex hose to hub in wellhead module. Made up clamp with Hy-torq kit." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.8 hours. Operational details: Removed hatches and transferred flowline support bracket to XMT deck. Installed hatches" "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Removed DHPG wellhead outlet. Cut and reterminated DHPG conductor. Replaced seals and re-installed DHPG wellhead outlet according to WD procedure. Tested wellhead outlet through exit block to 345 bar / 10 min - ok. Hooked up DHPG to wellhead junction box. Found that flow spool on XMT had wrong allignement." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Broke bolts on flowline spool. Re-alligned flowline spool." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Installed flowline hub support bracket on XMT. Found that it was the wrong bracket, even though it was marked F-14." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.8 hours. Operational details: Reverted to testing hydraulic control lines. Hooked up BOT pump. Tested DHSV line and exit block to 570 bar / 15 min - ok. Tested ASV line and exit block to 570 bar / 15 min - ok." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Removed chain hoists and slings from flowlines and repalced with 5 MT chainhoists and slings." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Removed wellhead bracket from XMT and put on weatherdeck. Meanwhile cut bolt holes in F-14 support bracket in mechanical workshop." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Rigged chainblocks and slings in moonpool for supporting tugger when pulling in coflex flowline Made up bolts on flow spool with Hy-torq kit." "On 2008-06-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Pulled/jacked coflex flowline hose using chain hoists, slings and tugger from drillfloor. Brought modified support bracket to XMT deck. Installled support bracket on XMT. Meanwhile serviced fwd PRS." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Jacked coflex flowline hub in place and made up graylock clamp with handtools." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Made up bolts on graylock clamp with Hy-torq kit. Attmepted to fit support bracket shoe/clamp - observed to narrow angle/gap between support bracket and shoe/clamp. Discussed situation- decided to continue operation as modification of the shoe/clamp would be needed. Suspended flowline in 2 ea 5 MT slings/chainhoists. Removed tugger from flowline. Removed kill line on F-12 and moved to F-14. Flushed packer fluid from cement unit and displaced line to drillwater. Pulled hydraulic line from well control panel to XMT deck. Installed hatches and cover. Meanwhile serviced TDS and drawworks." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Held toolbox talk prior to XMT bodytest and filling coflex flowline. Lined up cement unit. Performed line test against closed kill wing valve 30/345 bar 5 /10 min - ok. Opened kill wing valve, hydraulic master valve and manual master valve. Vented flowline on flow spool. Performed body test of XMT to 30/345 bar 5/10 min - ok. Lined up for filling coflex flowline from cement unit." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Lined up for filling coflex flowline. Filled coflex flowline with drillwater pumping from cement unit via KWV and HWV on XMT." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Held handover meeting / toolbox. Prepared for pulling dart and BPV." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Made up BPV retrieval rod. Pulled BPV and dart." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Transferred Well Dynamics pump to wellhead. Ran DHSV control hose from hydraulic panel in moonpool." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.0 hours. Operational details: Performed line test agains KWV to 30 bar / 5 min - ok. Attempted to test coflex flowline to 99 bar. Pressured up on cement unit. Walked lines and observed leakage in production manifold system. Meanwhile prepared for running WL." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 3.0 hours. Operational details: Attached hydrualic control hoses from well control panel to DHSV exit block and HMV actuator. Made up WD chemical injection manifold on wellhead. Re-arranged WD test pump and hooked up to checmical injection mainfold. Opened KWV and HMV from local control panel. Meanwhile prepared for running WL." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.2 hours. Operational details: Pressured up tubing to 35 bar and opened DHSV. Continued to pressure up on tubing to 220 bar / (750 liters). Closed LMV and bled off pressure above to 5 bar. Observed inflow test for 10 min - ok. Pressured up chemical injection line while maintaining pressure on tubing - held test for 10 min - ok. Equalize across LMV and opened same. Meanwhile prepared for running WL." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Closed HMV and bled off pressure above to 5 bar. Inflow tested HMV for 10 min - ok." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Bled of tubing pressure while maintaining pressure on chemical injection line. Observed rupture disc shearing at 70 bar tubing pressure. Chemical injection line pressure stabilized at ~50 bar. Pressured up on tubing to 100 bar to confirm checmical injection check valve holding - ok." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.2 hours. Operational details: Closed KWV, SHV and HMV. Rigged down testing equipment." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 0.5 hours. Operational details: Installed XMT cap." "On 2008-06-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 7.8 hours. Operational details: Commissioned XMT. Meanwhile prepared for running WL : -Re-arranged toolcatcher -Bulit grease injection -Built cable head -Checked and tested equipment" "On 2008-07-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Comissioned XMT. Tested coflex hose 100 bar / 15 min - test approved by production. Meanwhile prepared for running WL : -Changed IBOP on TDS -Performed service on drawwork -Cleaned and tidied drillfloor -Removed support bracket from flowline for modifications -Checked and tested equipment -Made up lubricator sections on cantilever -Spotted grease injection skid and well control skid on drillfloor" "On 2008-07-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Commissioned XMT. Meanwhile : -Dismantled IBOPs -Maintenance on diverter -Mounted and commissioned manrider on drillfloor -Cleaned lower shakers -Performed derrick inspection" "On 2008-07-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.0 hours. Operational details: Commissioned XMT. Meanwhile : -Installed WL riser spool / x-over on XMT. -Installed WL BOP's -Fitted hole cover around WL riser spool on weatherdeck" "On 2008-07-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 11.0 hours. Operational details: Commissioned XMT. Meanwhile : -Mounted IBOPs -Prepared for running WL -Cleaned in drilling areas" "On 2008-07-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 6.0 hours. Operational details: Commissioned XMT. Meanwhile : -Tested IBOP.s to 30345 bar 5/10 min - ok -Spotted WL BOP control unit -Built sacffolding around WL BOPs in moonpool -Hooked up and functioned WL BOPs -Ran WL riser and connected to WL BOPs -Tested/checked WL logging tools and WL tractor -Rigged lo-torques and check valve on F-14 XMT" "On 2008-07-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 18.0 hours. Operational details: Commissioned XMT. Meanwhile : -Cleaned drillfloor -Maintenance on diverter -Tidied in moonpool and wellhead module -Cleaned sackstore, pumproom and lower shakers -Rigged slings for WL sheaves" "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 2.8 hours. Operational details: Commissioned XMT. Meanwhile : -Cleaned drillfloor -Maintenance on diverter" "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to pressure testing WL rig up." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Lined up cement unit. Performed line test against KWV on XMT 30/345 bar 5/10 min - ok. Bled off pressure in line to cement unit. Bled off pressure in XMT to closed drain." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Hooked up local control on XMT. Removed hydraulic tube from HMV and drained hydraulic fluid. Hooked up and tested DHSV control hose to hose on XMT, tested to 520 bar / 10 min - ok. Hooked up HMV control hose and valve block. Had problems with leaking fitting on instrument valve block on HMV control hose. Reterminated fitting and tested hose 207 bar / 15 min - ok." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Leak tested rig up to rig floor to 30/185 bar 5/10 min using cmt pump and packer fluid. Ok. Bled off pressure to zero. Meanwhile held tool box talk for PU WL lubricator." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.8 hours. Operational details: Lifted in pre-made lubricator assembly from cantiliver to rig floor using crane and conveyer belt. Lifted lubricator vertically using T-bar in TDS and lifting slings. RU Welltech WL-tractor assembly in lower riser and GR-CCL, shock absorber and cable head in upper riser. MU entire toolstring and lifted into toolcatcher. MU lubricator to lower riser." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Opened SV (43 turns) and filled riser and lubricator with packer fluid using cmt pump. Meanwhile hoisted down bracket from XMT" "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Leak tested rig up to 30/185 bar 5/10 min using cmt pump and packer fluid. Ok." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Drained riser and flushed lines from cmt unit to closed drain with MEG." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: Worked to free WL toolstring from toolcatcher." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Lowered orientating weight and 30 ft gun section into lower riser section and hung off in C-plate. Filled riser with 200 ltrs of Ramex. Connected and armed perforating guns according to Schlumberger procedure." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Filled riser/lubricator with 180 ltrs of 100% MEG using cmt unit. Leak tested in-situ sub to 30/185 bar 5/10 min using Seawell pumpe and 100% MEG. Ok." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Open HMV and SV (43 turns). Equalized and opened DHSV. RIH with BHA #1 to perforate interval #1 from surface to 250 m. Powered up logging unit with guns 70 m below seabed." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3082m. The activity was categorized as 'workover -- wire line' and lasted for 3.5 hours. Operational details: RIH with BHA #1 from 250 to 3081,5 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open. Up weigh 480kg / hanging weight 466 kg at 493 m MDRT. Weights while RIH was according to tension simulations. Correlated and adjusted depth by 1 m before starting tractor." "On 2008-07-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Powered up WL tractor and continued RIH with BHA #1 to perforate interval #1 from 3081,5 to 3400 m. Running speed 12 m/min." "On 2008-07-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'workover -- perforate' and lasted for 0.8 hours. Operational details: Performed correlation log from 3400 m to 3200 m. Powered up WL tractor and ran back down to 3400 m. Schlumberger tools would not operate properly." "On 2008-07-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'interruption -- other' and lasted for 5.2 hours. Operational details: Trouble shoot power problem with downhole tools. Could not operate GR and switches, but were able to operate WL tractor. Attempted to locate error in surface system." "On 2008-07-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Continued to trouble shoot power problem with downhole tools. Could not operate GR and switches, but were able to operate WL tractor." "On 2008-07-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 3.0 hours. Operational details: POOH with BHA #1 from 3400 m to 250 m. Powered down logging unit with guns 70 m below seabed. Closed DHSV, HMV and SV. Broke lubricator at in-situ sub and LD toolstring." "On 2008-07-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 6.0 hours. Operational details: Continiued to trouble shoot power problem with toolstring. Had same problem with tools at surface. Found lower part of Welltec tractor drained for hydraulic oil. This may have affected tools below because the power situation in the toolstring was altered." "On 2008-07-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 2.0 hours. Operational details: MU and installed BHA #2 to perforate #1 with back-up WL tractor, back-up GR tool (non-modified PGGT) and changed out Schlumberger switches. Unable to move toolstring due to power shut down on WL winch." "On 2008-07-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 4.5 hours. Operational details: Made and installed new re-set handle for WL winch 380 V power supply. Trouble shoot problem with power supply." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.5 hours. Operational details: Continued trouble shooting problem with power supply and found loose rele. Fastened rele and installed ex-cover on WL winch." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: Lowered orientating weight and 30 ft gun section into lower riser section and hung off in C-plate. Filled riser with 200 ltrs of Ramex. Connected and armed perforating guns according to Schlumberger procedure." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 2.0 hours. Operational details: Leak tested in-situ sub to 30/185 bar 5/10 min using Seawell pumpe and 100% MEG. Ok. Bled down grease pressure and filled riser/lubricator with 253 ltrs of 100% MEG using cmt unit. Unable to start RIH with BHA #1 due to power shut down on WL winch." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.5 hours. Operational details: Trouble shoot problem with power supply on WL winch." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 233m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Open HMV and SV (43 turns). Equalized and opened DHSV. RIH with BHA #2 to perforate interval #1 from surface to 233 m. Powered up logging unit with guns 70 m below seabed." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3122m. The activity was categorized as 'interruption -- other' and lasted for 3.0 hours. Operational details: RIH with BHA #2 from 233 to 3122 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open. Up weigh 480kg / hanging weight 466 kg at 493 m MDRT. Weights while RIH was according to tension simulations. Correlated and adjusted depth by 1 m before starting tractor." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Powered up WL tractor and continued RIH with BHA #2 to perforate interval #1 from 3122 to 3400 m. Running speed 12 m/min." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Performed correlation log from 3400 m to 3200 m using GR. Powered up WL tractor and ran back down to 3400 m." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3358m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Fired guns and perforated interval #1, from 3345 - 3354.2 m MDRT. Good indication of firing on DHPG." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2560m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Performed GR-CCL log from 3266 m to 2450 m MDRT." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: POOH with BHA #1 from 2450 m to 250 m. Powered down logging unit with guns 70 m below seabed. Closed HMV and SV." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Broke lubricator at in-situ sub and LD toolstring." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Opened KWV and HMV and attempted to bullehead baseoil using cmt unit. Stopped when pressure reached 100 bar at 80 lpm. 2.9 m3 baseoil pumped in total. Meanwhile performed surface checks on Wellteck tractor and removed PGGT and chock absorber from toolstring." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Continued to perform surface checks on Welltech tractor. Lost contact with Schlumberger logging unit. Meanwhile held time-out for safety with drill crew with focus on the dropped object." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 1.0 hours. Operational details: Schlumberger unit experienced power shut down and had to restart all systems." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Went through Schlumberger and Welltech checklists. Checked CCL and gun switches." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: MU and installed BHA #3 to perforate interval #2." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Lowered orientating weight and 30 ft gun section into lower riser section and hung off in C-plate. Filled riser with 200 ltrs of Ramex. Connected and armed perforating guns according to Schlumberger procedure." "On 2008-07-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Leak tested in-situ sub to 30/150 bar 5/10 min using Seawell pumpe and 100% MEG. Ok." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Bled down grease pressure and filled riser/lubricator with 250 ltrs of baseoil using cmt unit." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 236m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Open HMV and SV (43 turns). Equalized and opened DHSV. RIH with BHA #3 to perforate interval #2 from surface to 236 m. Powered up logging unit with guns 70 m below seabed." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3120m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: RIH with BHA #3 from 236 to 3157 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open. Up weigh 480kg / hanging weight 465 kg at 493 m MDRT. Weights while RIH was according to tension simulations. Correlated and adjusted depth by 1 m before starting tractor." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Powered up WL tractor and continued RIH with BHA #3 to perforate interval #2 from 3157 to 3400 m. Running speed 12 m/min." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Performed correlation log from 3400 m to 2975 m using CCL. Powered up WL tractor and ran back down to 3400 m. Fired guns and perforated interval #2, from 3312 - 3321.2 m MDRT. Good indication of firing on DHPG." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: POOH with BHA #3 from 3309.7 m to 250 m. Powered down logging unit with guns 70 m below seabed. Closed DHSV, HMV and SV." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Broke lubricator at in-situ sub and LD toolstring." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Opened KWV and HMV and bullheaded 17.2 m3 baseoil at 137 lpm / 99.6 bar using cmt unit. Shut down pumps and observed pressure levelled out at 19 bar. Closed HMV. Bled down pressure above and inflow tested HMV. Ok. Meanwhile performed torture test on logging cable. Cut off 60 m of cable and rebuilt cable head." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Continued building cable head and performed surface checks on Wellteck tractor." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Continued to perform surface checks on Welltech tractor. Went through Schlumberger and Welltech checklists. Meanwhile installed test cap on lubricator. Opened KWV and pumped up to 19 bar above HMV using baseoil and cmt unit. Tested SV to 19 bar / 5 min. Opened HMV and read 19 bar WHP, 255 bar on DHPG. Displaced cmt line to 100% MEG at 50 lpm / 49 bar and got a final WHP of 20 bar. Closed HMV and bled off pressure to 5 bar above. Inflow tested HMV for 10 min. Ok. Bled off pressure above HMV and closed KWV and LT2." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Continued to go through Schlumberger and Welltech checklists. Checked CCL and gun switches." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Installed BHA #4 to perforate interval #3. Lowered orientating weight and 30 ft gun section into lower riser section and hung off in C-plate. Filled riser with 200 ltrs of Ramex. Connected and armed perforating guns according to Schlumberger procedure." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Leak tested in-situ sub to 30/150 bar 5/10 min using Seawell pumpe and 100% MEG. Ok. Bled down grease pressure and filled riser/lubricator with 250 ltrs of 100% MEG using cmt unit." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Performed time-out for safety with focus on dropped object. Pressured up to 20 bar and equalized pressure above HMV.Open HMV and SV (43 turns). Equalized and opened DHSV. RIH with BHA #4 to perforate interval #3 from surface to 235 m. Powered down logging unit with guns 70 m below seabed." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2500m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: RIH with BHA #4 from 235 to 2500 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open. Weights while RIH was according to tension simulations. Schlumberger was unable to communicate with gun switches." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1500m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Trouble shoot problem with gun switches. POOH with BHA #4 from 2500 m to 1500 m and re-tried to communicate with the switches, because they worked at this depth while RIH. Negative." "On 2008-07-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH with BHA #4 from 1500 m to 250 m. Powered down logging unit with guns 70 m below seabed." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 86m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Continued to POOH with BHA #4 from 250 m to 86 m. Unable to move toolstring due to power shut down on WL winch." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 86m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Electrican opened ex-panel and re-sat main switch." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 17m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Continued to POOH with BHA #4 from 86 m to 17 m. Unable to move toolstring due to power shut down on WL winch." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 17m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Electrican opened ex-panel and re-sat level sensor." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.8 hours. Operational details: Continued to POOH with BHA #4 from 17 m to OOH. Closed SV and HMV. Inflow tested HMV to 20-5 bar/10 min. Ok. Bled off pressure. Held tool box meeting prior to LO guns and tractor. Cleaned rig floor due to slipping hazard. Broke lubricator at in-situ sub and hung off gun in riser." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Trouble shoot problem with gun switch and found faulty switch. Changed to back-up switches. Checked toolstring with tractor and switches installed." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: LO guns and WL tractor. Checked WL tractor oil level." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: Continued to perform checkes on WL tractor. Lifted WL tractor on to drill floor. Meanwhile cleaned drillfloor." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: MU and installed BHA #5 to perforate interval #3. Lowered orientating weight and 30 ft gun section into lower riser section and hung off in C-plate. Drained riser and filled it with 200 ltrs of Ramex. Connected and armed perforating guns according to Schlumberger procedure. Leak tested in-situ sub to 30/150 bar 5/10 min using Seawell pumpe and 100% MEG. Ok." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Bled down grease pressure and filled riser/lubricator with 250 ltrs of 100% MEG using cmt unit. Pressured up to 20 bar and equalized above HMV." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 235m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Open HMV and SV (44 turns). 19.6 bar WHP and 255 bar on DHPG. RIH with BHA #5 to perforate interval #3 from surface to 235 m. Powered up logging unit with guns 70 m below seabed." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2500m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: RIH with BHA #5 from 235 to 2500 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3180m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH with BHA #5 from 2500 to 3180 m. PU 50 m every 500 m due to new cable. Weights while RIH was according to tension simulations. Correlated and adjusted depth before starting tractor." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3330m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Powered up WL tractor and continued RIH with BHA #5 to perforate interval #3 from 3180 to 3330 m. Running speed 11 m/min." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3400m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Performed correlation log from 3330 m to 2975 m using CCL. Had 10 min power shut-down on WL winch. Powered up WL tractor and ran back down to 3330 m. Fired guns and perforated interval #3, from 3287 - 3296.2 m MDRT. Good indication of firing on DHPG." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: POOH with BHA #5 from 3250 m to 250 m. Powered down logging unit with guns 70 m below seabed." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Continued to POOH with BHA #5 from 250 m to OOH. Closed SV and HMV. Bled off XMT cross to 5.8 bar. Inflow tested HMV to 20-5.8 bar/10 min. Ok. Bled off pressure and drained riser. Cleaned rig floor due to slipping hazard." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Held tool box meeting prior to LO guns and tractor. Broke lubricator at in-situ sub and LD guns and toolstring." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Held tool box meeting before LD lubricator. LD lubricator on drill floor and removed tool catcher for Welltec cable head." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 2.0 hours. Operational details: Inspected grease head and line wiper. Found kink on return hose and missing plug for grease head. Changed out grease return system on grease head." "On 2008-07-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Installed tool catcher for Schlumberger cable head." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Continued to install tool catcher for Schlumberger cable head." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Built new cable head on 7/16' cable for BHA #6. Checked CCL and toolstring. Prepared to RU lubricator. Meanwhile trouble shoot bleed off valve on grease skid." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Held tool box meeting and PU lubricator to vertical position on rig floor. Observed incorrect installation of hoses on lubricator." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 0.5 hours. Operational details: LD lubricator and re-arranged hoses." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: PU lubricator to vertical position on rig floor. MU lubricator to lower riser." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Filled riser with 450 ltrs 100% MEG and pressure tested rig up to 30/185 bar 5/10 min. Ok. Broke lubricator at in-situ sub and checked CCL." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: MU and installed BHA #6 to perforate interval #4. Lowered orientating weight, 20 ft gun section and 30 ft gun section into lower riser section and hung off in C-plate. Filled it with 185 ltrs of Ramex. Connected and armed perforating guns according to Schlumberger procedure. Leak tested in-situ sub to 30/150 bar 5/10 min using Seawell pump and 100% MEG. Ok." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Bled down grease pressure and filled riser/lubricator with 280 ltrs of 100% MEG using cmt unit. Pressured up to 20 bar and equalized above HMV. Drain hose on lubricator parted." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 0.5 hours. Operational details: Re-united and fixed splize on drain hose on lubricator." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Open HMV and SV (44 turns). 22.2 bar WHP and 256 bar on DHPG. RIH with BHA #6 to perforate interval #4 from surface to 235 m. Powered up logging unit with guns 70 m below seabed." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3100m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: RIH with BHA #6 from 235 to 3100 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3075m. The activity was categorized as 'workover -- perforate' and lasted for 1.0 hours. Operational details: Performed correlation log from 3100 m to 2975 m using CCL. Ran back down to 3048 m. Fired guns and perforated interval #4, from 3044 - 3059.2 m MDRT. Good indication of firing on DHPG." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH with BHA #6 from 3250 m to 250 m. Powered down logging unit with guns 70 m below seabed." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Continued to POOH with BHA #5 from 250 m to OOH. WHP 33.7 bar and 263 bar on DHPG. Closed SV and HMV. Bled off XMT cross to 5.3 bar. Inflow tested HMV to 20-5.3 bar/10 min. Ok. Bled off pressure and flushed riser/lubricator with nitrogen. Cleaned rig floor due to slipping hazard." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Held tool box meeting prior to LO guns and tractor. Isolated gas detector on rig floor. Broke lubricator at in-situ sub and LD guns and toolstring. All shots fired." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.8 hours. Operational details: Changed to backup head without rebuilding rope socket, due to ECRD weak point. Checked CCL and toolstring." "On 2008-07-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: MU and installed BHA #7 to perforate interval #5. Lowered 30 ft gun section into lower riser section and hung off in C-plate. Connected and armed perforating gun according to Schlumberger procedure." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: MU and installed BHA #7 to perforate interval #5. Lowered orientating weight and 20 ft gun section into lower riser section and hung off in C-plate. Connected and armed perforating guns according to Schlumberger procedure. Filled it with 180 ltrs of Ramex. Leak tested in-situ sub to 30/150 bar 5/10 min using Seawell pumpe and 100% MEG. Ok." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Bled down grease pressure and filled riser/lubricator with 270 ltrs of 100% MEG using cmt unit. Pressured up to 34 bar and equalized above HMV." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 255m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Open HMV and SV (44 turns). 42.3 bar WHP and 267 bar on DHPG. RIH with BHA #7 to perforate interval #5 from surface to 255 m. Powered up logging unit with guns 70 m below seabed." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3055m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: RIH with BHA #7 from 255 to 3055 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open. Had 10 min power shut-down on WL winch. Had to use Schlumberger tension and depth system due to software problem in WL winch." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3050m. The activity was categorized as 'workover -- perforate' and lasted for 0.5 hours. Operational details: Performed correlation log from 3050 m to 2975 m using CCL. Ran back down to 3050 m. Adjusted brakes on WL winch. Fired guns and perforated interval #5, from 3021 - 3036.2 m MDRT. Good indications of firing." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH with BHA #7 from 3250 m to 250 m. Powered down logging unit with guns 70 m below seabed." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Continued to POOH with BHA #7 from 250 m to OOH. WHP 46.2 bar and 265 bar on DHPG. Closed SV and HMV. Bled off XMT cross to 5 bar. Inflow tested HMV to 46-5 bar/10 min. Ok. Bled off pressure and flushed riser/lubricator with nitrogen." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Held tool box meeting prior to LO guns. Broke lubricator at in-situ sub and LD guns and toolstring. All shots fired." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Changed to backup head without rebuilding rope socket, due to ECRD weak point. Checked CCL and toolstring." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: MU and installed BHA #8 to perforate interval #6. Lowered 30 ft gun section, orientating weight and 20 ft gun section into lower riser section and hung off in C-plate. Connected and armed perforating guns according to Schlumberger procedure. Filled it with 180 ltrs of Ramex." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Bled down grease pressure and filled riser/lubricator with 270 ltrs of 100% MEG using cmt unit. Pressured up to 46 bar and equalized above HMV. Leak tested in-situ sub to 30/150 bar 5/10 min using Seawell pumpe and 100% MEG. Ok." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Open HMV and SV (44 turns). 50 bar WHP and 267 bar on DHPG. RIH with BHA #8 to perforate interval #6 from surface to 250 m. Powered up logging unit with guns 70 m below seabed." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3040m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: RIH with BHA #8 from 250 to 3040 m. PU 50 m every 500 m due to new cable. Ran carefully through DHSV and pulled back up to confirm that it was fully open." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3040m. The activity was categorized as 'workover -- perforate' and lasted for 1.8 hours. Operational details: Performed correlation log from 3040 m to 2975 m using CCL. Had problems running back down to 3040 m because toolstring stopped in previous perforation interval #5, 3021-3036.2 m." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3040m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Seawell failed to stop on shooting depth twice and another correlation run had to be made because the guns had become off depth in the attempts." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3040m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Fired guns and perforated interval #6, from 3005 - 3020.2 m MDRT. Good indications of firing." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1562m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: POOH with BHA #8 from 2980 m to 1562 m. Unable to move toolstring due to power shut down on WL winch." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1562m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Electrican opened ex-panel and re-sat main switch." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 250m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: POOH with BHA #8 from 1562 m to 250 m. Powered down logging unit with guns 70 m below seabed." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Continued to POOH with BHA #8 from 250 m to OOH. WHP 67.3 bar and 267 bar on DHPG." "On 2008-07-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Held tool box meeting before operating valves due to new drilling- and production crews. Closed SV and HMV. Bled off XMT cross to 5 bar." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Inflow tested HMV to 67-5 bar/10 min. Ok. Bled off pressure. Opened KWV and equalized and opened HMV using 100% MEG and cmt unit. Closed DHSV. Bullheaded 3 m3 100% MEG followed by 6.3 m3 of basoil at 500 lpm / 77 bar. Bled off pressure above DHSV to 5 bar and inflow tested DHSV to 67-5 bar for 30 min. Ok. Bled off pressure above DHSV to zero." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Closed HMV. Flushed XMT, riser and lubricator with nitrogen to closed drain." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Held tool box meeting prior to LO guns. Broke lubricator at in-situ sub and LD guns and toolstring. All shots fired." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Closed all XMT valves. Cut 7/16' cable and started to RD WL lubricator on rig floor." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.0 hours. Operational details: RD lubricator and WL upper risers sections." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Removed scaffolding from WL BOP and shut down F-4 injection due to need of changing actuator." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: RD WL BOP's and placed below moonpool hatch. Removed lower riser sections from XMT and lifted to rig floor." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.8 hours. Operational details: Installed XMT tree cap. Transferred operation of HMV and DHSV from WL controlled panel to Mærsk production. Removed kill line hose and installed 1502 weco blind cap outside KWV." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Removed half moon hatch and lowered down actuator for F-4. Installed full hatch on F-14." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'completion -- bop/wellhead equipment' and lasted for 1.5 hours. Operational details: Leak tested tree cap, XMT cross and KWV cap to 35/345 bar for 5/10 min using Seawell pump and 100% MEG. Ok. Bled off pressure. Meanwhile removed WL BOP's from moonpool and performed skidding checks." "On 2008-07-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Performed well hand over activities. Verified that all valves on XMT and DHSV were closed. Meanwhile continued to remove WL equipment from rig floor. Handed well over to Maersk production at 18:00. ****************END OF OPERATIONS****************" "On 2009-03-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Re-arranged hatches on weather deck." "On 2009-03-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk prior to skidding from F-15 to F-14." "On 2009-03-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Removed scaffoling on Weather deck and bridge from production module to cantilever." "On 2009-03-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Skidded rig from F-15 to F-14. Made adjustments as required to put rotary in line with F-14 XMT." "On 2009-03-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 1.8 hours. Operational details: Waited on handover of well F-14. Meanwhile : -Landed WL riser/BOP on Weather deck hatch and secured same -Built scaffolding/rails on Weather deck -Performed general PMs in drilling areas -Dismantled drilling BOP -Re-terminated ROV umbilical" "On 2009-03-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 6.0 hours. Operational details: Waited on handover of well F-14. Meanwhile : -Performed general PMs in drilling areas -Dismantled drilling BOP -Re-terminated ROV umbilical -Performed checks on WL equipment" "On 2009-03-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 18.0 hours. Operational details: Waited on handover of well F-14. Meanwhile : -Worked on choke manifold valves -Bled of pressure on drilling BOP control system -PM on mudpump #3 -Changed valves XCV1/XC2 on trip tanks -Managed DROPS punch items in derrick -Performed general housekeeping in drillng areas" "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 6.0 hours. Operational details: Waited on handover of well F-14. Meanwhile : -Dismantled drilling BOP components" "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 13.0 hours. Operational details: Waited on handover of well F-14. Meanwhile : -Prepeared for WL operation -Dismantled drilling BOP components" "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Performed toolbox for commencing WL operations." "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Hooked up local control to HMV and DHSV. Shifted valve on HMV quick dump. Removed cap on KVW and rigged up bleed off line/manifold. Checked for pressure and removed treecap." "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Removed lid on WL hatch and came down with WL riser. Adjusted WL hatch a few inches to starboard due to clash with WL riser. Landed WL riser on top of XMT and made up quick union. Hooked up BOP and tested hoses / calibrated rams (function test) - ok." "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Lined up to flush cement line. Flushed line from cement unit to XMT with MEG taking returns through closed drain." "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Performed line test to 30/200 bar 5/10 min against closed KWV. Obtained test <1% drop 10 min. Bled off pressure to closed drain. Bled off pressure on production flowline and vented same for continued testing." "On 2009-03-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Installed cap on WL riser. Lined up and filled WL riser with MEG from cement unit. Filled riser until fluid returns through needle valve on riser cap." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Closed SV. Pressure tested XMT flowcross (PVW/HMV/SV) to 30/200 bar 5/10 min - ok. Bled off pressure to closed drain and closed KWV." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held toolbox talk for rigging up WL." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Lifted up WL lubricator and upper sheave. Rigged up lower sheave. Connected cable head to WL tractor and pulled same into lubricator. Built PLT toolstring using tugger. Stabbed PLT toolstring into WL riser and connected to WL tractor." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Performed electrical checks of PLT and WL tractor according to Schlumberger/Welltech procedures." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Made up quick union between WL riser and lubricator. Lined up to pump from cement unit. Filled lubricator with MEG. Pressure tested WL rig up to 30/200 bar 5/10 min - ok. Bled off pressure to cement unit and inflow tested check valve in bleed off line to 200 bar differential - ok. Meanwhile held wellcontrol drill/brief and toolbox talk prior to RIH. Bled off pressure to 20 bar to closed drain. Closed KWV. Opened HMV, pressure above DHSV 0,5 bar. Opened KVW." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Pumped MEG to equalize across DHSV. Pumprate 130 l/min." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 22m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Pumped MEG to equalize DSHV. Pumprate 130 lpm. Got pressure build up and pressure levelled out at 103,9 bar. Total volume pumped 6,3 m3. Equalised across SV with Seawell pump and opened same. Closed KWV and bled down pressure on line to closed drain." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with PLT/tractor toolstring on 7/16' EWL from 22 m to 500 m MD. Ran carfully through DHSV at 492 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 500m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Performed toolbox talk/handover meeting. Conducted well control drill." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2543m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: RIH with PLT/tractor toolstring on 7/16' EWL from 500 m to 2543 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2982m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with PLT/tractor toolstring on 7/16' EWL from 2543 m to 2982 m MD. Correlated depth against reference log." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Performed PLT calibration passes from 2840 m to 2900 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3092m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH with PLT/tractor toolstring on 7/16' EWL from 2900 m to 3092 m MD. Not able to progress further with out tractor." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Powered up tractor and RIH with PLT/tractor toolstring on 7/16' EWL from 3092 m to 3395 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: POOH with PLT/tractor toolstring on 7/16' EWL from 3395 m to 2950 m MD. Took stationary PLT readings at : 3333 m MD 3304 m MD 3173 m MD 3040 m MD 2950 m MD No x-flow recorded." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3057 m MD and powerd up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3057 m to 3395 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 10 m/min." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3006 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3006 m to 3395 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 20 m/min." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3005 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3005 m to 3395 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 30 m/min." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3016 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3016 m to 3395 m MD." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 30 m/min. Picked up to 2900 m MD. WL stand-by for flowing well. Equalised across and opened PVW." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Beaned up well in increments to 1500 Sm3/d. Got production shut down due to high level on separator." "On 2009-03-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wait' and lasted for 5.5 hours. Operational details: Waited on production department to start up production. Production on F-14 commenced at 23:15." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wait' and lasted for 0.8 hours. Operational details: Waited on production department to start up production." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 3.2 hours. Operational details: Produced well at 1600 Sm3/d. WL stand-by for flowing well / stabilizing FBHP (<0,1 bar variance 1 hr). Obtained stable FBHP of ~283 bar at DHPG." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: RIH to 2973 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 2973 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: POOH with PLT/tractor toolstring on 7/16' EWL from 3395 m to 2950 m MD. Took stationary PLT readings at : 3333 m MD 3304 m MD 3173 m MD 3040 m MD 2950 m MD" "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3038 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3038 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 10 m/min." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3033 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3033 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 20 m/min." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3049 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3049 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 30 m/min." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3053 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3053 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 40 m/min. Picked up to 2900 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 5.2 hours. Operational details: Beaned up well in increments to 3000 Sm3/d. WL stand-by for flowing well / stabilizing FBHP (<0,2 bar variance 1 hr). Obtained stable FBHP of ~273 bar at DHPG." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3001 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3001 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: POOH with PLT/tractor toolstring on 7/16' EWL from 3395 m to 2950 m MD. Took stationary PLT readings at : 3333 m MD 3304 m MD 3173 m MD 3040 m MD 2950 m MD" "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3005 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3005 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 10 m/min." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3017 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3017 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 20 m/min." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3057 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3057 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 30 m/min." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3082 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3082 m to 3395 m MD." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 40 m/min. Picked up to 2900 m MD. PLT data checked by PETEK engineer - ok." "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Beaned up well to 4000 Sm3/d. Meanwhile RIH to 3027 m MD. Took p/u weight at 10 m/min to verify simulations. P/u weight ~3100 lbs in correspondance with simulated values. Picked up to 2900 m MD" "On 2009-03-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Beaned up well to 4500 Sm3/d." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Beaned up well to 4500 Sm3/d. Meanwhile RIH to 3056 m MD. Took p/u weight at 10 m/min to verify simulations. P/u weight 3000-3100 lbs in correspondance with simulated values. Picked up to 2900 m MD. Had problems maintaining rate at 4500 Sm3/d due to high separator levels. Cut back rate to 4250 Sm3/d." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Allowed downhole pressure to stabilize at 4250 Sm3/d to <0,2 bar/hr FBHP variance. Obtained stable FBHP of ~267,5 bar at DHPG." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3027 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3027 m to 3395 m MD." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 40 m/min." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3038 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3038 m to 3395 m MD." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 30 m/min." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3060 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3060 m to 3395 m MD." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 20 m/min." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: RIH to 3030 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3030 m to 3395 m MD." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2950m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Made upwards logging pass from 3395 m to 2950 m MD at 10 m/min." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3395m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH to 3030 m MD and powered up tractor. RIH with PLT/tractor toolstring on 7/16' EWL from 3030 m to 3333 m MD." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3333m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: POOH with PLT/tractor toolstring on 7/16' EWL from 3333 m to 2950 m MD. Took stationary PLT readings at : 3333 m MD 3304 m MD 3173 m MD 3040 m MD 2950 m MD" "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2547m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: POOH with PLT/tractor toolstring on 7/16' EWL from 2950 m to 2547,5 m MD. Checked PLT sensors towards DHPG. Checked PLT data. Shut- in well." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 11m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: POOH with PLT/tractor toolstring on 7/16' EWL from 2547 m MD to surface. Ran carefully through DHSV at 492 m MD. Ran cable head into toolcatcher." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 11m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Closed SV partly and verified toolstring out of hole. Recorded SIWHP 120 bar. Closed HMV, bled down pressure above to 5 bar and inflow tested - ok. Bled off pressure to zero to closed drain and purged riser with Nitrogen. Lined up cement unit and filled riser with MEG. Closed SV and tested flow cross to 30/200 bar 5/10 min - ok. Hooked up permanent hydraulic controls to HMV and DHSV. Re-opened DHSV." "On 2009-03-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 11m. The activity was categorized as 'workover -- wait' and lasted for 9.5 hours. Operational details: Equalised across PVW and beaned up well. Stand by for rigging down WL until scheduled shut-in." "On 2009-03-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 11m. The activity was categorized as 'workover -- wait' and lasted for 6.0 hours. Operational details: Stand by for rigging down WL until scheduled shut-in." "On 2009-03-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 11.0 hours. Operational details: Stand by for rigging down WL until scheduled shut-in. Monitored lubricator and WL riser for pressure build up every 15 min. Meanwhile - prepared skid list - performed 5-yearly on choke manifold - dismantled hydraulic hoses on tension cylinders - cleaned wellhead and moonpool area. - screened slops" "On 2009-03-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: Waiting on MDN. Unable to proceed with WL operation due to ongoing 5-yearly work on tension cylinders in moonpool." "On 2009-03-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.5 hours. Operational details: Waited on Mærsk Production to shut in well and inflow test HMV to 119-5 bar/10 min and DHSV to 119-5 bar/30 min. Had 0.7 bar drop/10 min on HMV and 0.3 bar drop/30 min on DHSV. Bled off pressure to 0 bar above DHSV. Isolated HMV. Confirmed valve status and handed over well to drilling at midnight. Meanwhile cleaned in moonpool area and injected slop. Held tool box meeting for RD lubricator, LD toolstring and performe dual lift of WL riser. Sorted out problem with exhaust fumes on drillfloor." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.0 hours. Operational details: Released tool from tool catcher and verified no pressure in lubricator. Opened SV. Drained WL riser to closed drain and flushed with nitrogen." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Broke lubricator above in-situ sub and LD Schlumberger tools and Welltech tractor. No marks or damage to toolstring." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Ran cable through WL BOP and attempted to test to 20/345 bar for 5/10 min. Not able to pressure up to more than 160 bar. Ran test rod on rope through WL BOP and tested to 20/345 bar for 5/10 min using drill water. Ok." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: LD lubricator onto HTS to be able to change grease tubes while skidding." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Installed 10 MT lifting cap on WL riser and installed elevator on riser section." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Disconneced WL riser and BOP from XMT and lifted off with TDS. Secured lift with slips in rotary and kept suspended from rig floor." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: RU to move hatches in moonpool. Removed WL hatch and moved hatches 14, 13 and 12 to cover all openings on weather deck." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: RD surface lines from KWV. RU HP hose from cmt unit to KWV." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 4.2 hours. Operational details: Performed line test from KWV to cmt unit. Ok. Opened SV and KWV. Leak tested tree cap and XMT cross to 30/345 bar for 5/10 min using cmt unit. Ok. Bled off pressure. Closed SV. Leak tested SV to 30/345 bar for 5/10 min using cmt unit. Ok. Bled off pressure. Closed KWV and RD surface lines on KWV. Installed cap on KWV and removed 1/2' plug. Opened SV. Leak tested KWV to 30/345 bar for 5/10 min using Seawell pump. Ok. Bled off pressure. Opened KWV. Installed 1/2' plug in KWV cap. Leak tested KWV cap to 30/345 bar for 5/10 min using Seawell pump. Ok. Bled off pressure. Disconnected Seawell test pump from WH cap and closed needle valve." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: De-isolated HMV and re-established platform permanent control system. Filled in and signed 'Well handover document' and handed over well from Volve D&W to Mærsk Production at 14:00. Meanwhile held tool box talk for skidding from F-15 to F-12." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Removed stair cases from cantiliver to main deck and scaffolding in moonpool." "On 2009-03-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Skidded rig from F-14 4.5 m fwd to F-12. ***Operation transferrred to F-12***" "On 2010-09-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Spotted wire line equipment on cantilever deck." "On 2010-09-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.0 hours. Operational details: Hooked up electricity to Schlumberger logging unit and dog house. Meanwhile leak tested WL BOP on stump. Unpacked risers and grease head from rack." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.8 hours. Operational details: Made up Grease Injection Head with 7/16' cable.. Meanwhile moved WL BOP to moon pool area and started to hook up electricity to AWS equipment." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to assemble the lubricator and riser." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Assembled lubricator and riser on rig floor. Meanwhile built cable head and megged same." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Assembled lubricator and riser on rig floor." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 1.8 hours. Operational details: All personnel mustered to life boat drill and attended OIM's HSE meeting." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Prepared hoses for BOP, hooked up remote control unit in WL winch and completed lubricator." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 6.2 hours. Operational details: Tested PLT and 2 1/8' Tractor (Primary and back-up)." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Completed hook up of electric power to winch power pack." "On 2010-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 5.0 hours. Operational details: Hooked up hoses to GIH and prepared hoses for local control of HMV and DHSV, while production dept. prepared well for handover to well service." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Handed well over from production to well service. SIWHP 92 bar." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held tool box meeting prior to test of x-mas tree and installation of manifold on TKV." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: Waited on production dept. for activation of work permit." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Leak tested x-mas tree to 20/ 170 bar for 5/ 10 min, against HMV, PWV, TKV and SV." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Installed manifold on TKV and leak tested same to 20/ 170 bar for 5/ 10 min, against TKV." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Held tool box meeting prior to removing tree cap and R/U of riser and BOP." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.0 hours. Operational details: Removed tree cap and rigged up riser and BOP." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Leak tested connections between BOP and XMT as well as LTV and bleed off hose outside TKV. All tests done to 20/170 bar for 5/10 min." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Held tool box talk and hoisted down upper riser through RT and stabbed same onto BOP. Installed upper sheave wheel with 7/16' cable and hoisted up lubrikator and GIH in elevator. Lifted up tractor and hung off in riser. WL winch suddenly stopped. Unable to find and correct problem. LD tractor." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- rig up/down' and lasted for 5.8 hours. Operational details: Troubleshot winch problem, Mærsk electrician assisted. Bypassed relay, restarted power pack and let it run for two hours without any problem. Decided to continue acc. to program." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Made up BHA # 1 with PLT and 2 1/8' Tractor, stabbed on lubricator and lined up for filling of rig-up with productions MEG pump." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.5 hours. Operational details: Held tool box meeting prior to test of rig-up." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.2 hours. Operational details: Filled rig-up using productions MEG pump. Leak tested rig-up to 20/ 170 bar for 5/ 10 min." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Held pre-job meeting and reviewed program for PLT logging with involved personnel." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.8 hours. Operational details: Opened HMV and pumped 6,5 m³ of MEG to equalize and open DHSV." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.2 hours. Operational details: Equalized and opened Swab valve. SIWHP 75,8 bar, DHPG 292,5 bar and DHTG 102,3 deg C." "On 2010-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 150m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH with PLT/ RST logging tool and tractor at 10 m/ min to 150 m." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 450m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Continued to RIH with PLT/ RST logging tool and tractor at 10 m/ min. Increased speed to 20 m/ min at 300 m MDRKB." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 450m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Stopped at 450 m MDRKB and powered up minitron and checked tools." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2556m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Continued to RIH with PLT/ RST logging tools and tractor at 40 m/ min." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2675m. The activity was categorized as 'workover -- perforate' and lasted for 0.2 hours. Operational details: Performed depth correlation across interval 2556 - 2675 m MDRKB." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2542m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Positioned PLT at P/T sensors in DHG at 2542 m MDRKB. PLT readings: 4242,9 psi (292,55 bar), 102 deg C. DHG readings: 292,56 bar, 102,22 Deg C." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Performed spinner calibration across interval 2850-2900 m MDRKB at 10, 20, 30 and 40 m/ min up/down." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Verified inline and full bore spinner calibration and positioned full bore spinner at 2900 m MDRKB. SIWHP 74,9 bar, DHP 292,59 bar, DHT 102,14 deg C." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Equalized and opened PWV." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Started to bean up well to test separator. At 06:00 hrs: Choke 19%, FWHP 64 bar, DHP 285,3 bar, DHT 105,6 deg C." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 4.2 hours. Operational details: Continued beaning up well until choke size at 40,2 %. Stabilized flow rate at appr. 5200 Sm³/d." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3380m. The activity was categorized as 'workover -- wire line' and lasted for 4.8 hours. Operational details: RIH 30 m and tool string stopped. Started tractor and RIH to 3380 m. Logged flowing up-passes with PLT tools between 3380 and 2970 m at 10/20/30/40 m/min. Tractored down each time. Took stationary readings at 3200, 3040 and 2970 m. Positioned tool string with full bore spinner at 2900 m." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Choked back flow rate to 3300 Sm³/d and stabilized." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3380m. The activity was categorized as 'workover -- wire line' and lasted for 4.5 hours. Operational details: Started tractor and RIH to 3380 m. Logged flowing up-passes with PLT tools between 3380 and 2970 m at 10/20/30/40 m/min. Tractored down each time. Took stationary readings at 3200, 3040 and 2970 m. Positioned tool string with full bore spinner at 2900 m." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2900m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Choked back flow rate to 1800 Sm³/d and stabilized." "On 2010-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3380m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Started tractor and RIH to 3380 m." "On 2010-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2970m. The activity was categorized as 'workover -- wire line' and lasted for 4.0 hours. Operational details: Logged flowing up-passes with PLT tools between 3380 and 2970 m. Tractored down each time. Took stationary readings at 3200, 3042 and 2970 m." "On 2010-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2970m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Choked back and shut in well on PWV. SIWHP 93,9 bar, DHP 293,5 bar, DHT 105,7 deg C." "On 2010-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3642m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Started tractor and RIH to 3642 m." "On 2010-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3637m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Powered up minitron source and started to log up with RST in IC mode at 0,5 m/min." "On 2010-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3103m. The activity was categorized as 'workover -- wire line' and lasted for 18.0 hours. Operational details: Continued logging RST in IC mode at 0,5 m/min." "On 2010-09-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2975m. The activity was categorized as 'workover -- wire line' and lasted for 5.2 hours. Operational details: Continued logging RST in IC mode at 0,5 m/min up to 2975 m." "On 2010-09-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3642m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Started tractor and RIH to 3642 m." "On 2010-09-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3642m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Powered up minitron source." "On 2010-09-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3150m. The activity was categorized as 'workover -- wire line' and lasted for 18.0 hours. Operational details: Logged RST in IC mode at 0,5 m/min from 3642 to 3150 m." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3098m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Logged RST in IC mode at 0,5 m/min from 3150 to 3101 m. RST far detector stopped working." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3116m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Tractored back into well 15 m and stopped at 3116 m. Troubleshot and made several attempts to get the detector to work. Neg." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3390m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH with tractor activated to 3390 m." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2970m. The activity was categorized as 'workover -- wire line' and lasted for 0.8 hours. Operational details: Ran PLT logging pass from 3390 m up to 2970 m at speed 10 m/min." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3390m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: RIH with tractor activated to 3390 m." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2970m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Ran PLT logging pass from 3390 m up to 2970 m at speed 20 m/min." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3390m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with tractor activated to 3390 m." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2970m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Ran PLT logging pass from 3390 m up to 2970 m at speed 30 m/min." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3390m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with tractor activated to 3390 m." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2970m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Ran PLT logging pass from 3390 m up to 2970 m at speed 40 m/min." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3200m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH with tractor activated to 3200 m." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2970m. The activity was categorized as 'workover -- wire line' and lasted for 1.2 hours. Operational details: Took stationary readings at 3200, 3040 and 2970 m. Evaluated data." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: POOH with BHA #1. Lost communication with PLT/RST on the way OOH." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: OOH. SIWHP 103 bar. Closed well and bled off pressure. Flushed riser/lubricator with N2. Inflow tested HMV. LD BHA #1." "On 2010-09-16, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 10.8 hours. Operational details: Waited on plug equipment from shore. Boat departure cancelled due to poor weather forecast. Meanwhile produced well and prepared 5/16' cable equipment due to loose strand on 7/16' cable." "On 2010-09-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on plug equipment from shore. Meanwhile produced well and prepared 5/16' cable equipment." "On 2010-09-17, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 18.0 hours. Operational details: Waited on plug equipment from shore. Meanwhile produced well and prepared 5/16' cable equipment. Rigged up lubricator with grease inj. head. Function tested tractor through cable. Held SJA meeting regarding RD of wireline equipment and skidding preparations." "On 2010-09-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 6.0 hours. Operational details: Waited on plug equipment from shore. Meanwhile produced well. Held SJA meeting regarding RD wireline equipment and prepare for skidding." "On 2010-09-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 9.5 hours. Operational details: Waited on plug equipment from shore. Meanwhile produced well. Held pre-job meeting with involved personnel." "On 2010-09-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.5 hours. Operational details: Received plug equipment from boat. Unloaded basket and checked DPU. Transferred plug to drill floor with rig crane (appr. 125 kg)." "On 2010-09-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 1.0 hours. Operational details: Closed in well. Meanwhile held prejob meeting with all personnel involved regarding RU BHA, install plug and RD WL equipment." "On 2010-09-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Took over controll of HMV and DHSV. Opened WL BOP. Installed BHA#2 into lubricator. Added 50 litres of Ramex into riser. Leak tested rig up. 20/170 bar for 5/10 min. Pumped totally 700 litres. Opened well. WHP = 97.5 bar." "On 2010-09-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 490m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: RIH with BHA#2, EVO plug on tractor. Stopped into DHSV. Attempted several times to pass. Neg." "On 2010-09-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 490m. The activity was categorized as 'workover -- wire line' and lasted for 0.5 hours. Operational details: Started to equalize DHSV by pumping MEG into well." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 490m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Continued pumping MEG into well to equalize DHSV. Pressure increased from 97,5 bar to 100 bar." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 525m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: RIH with BHA #2 and passed DHSV. Stopped in Baker AVLDM tubing hanger at 510 m. Had to work BHA from 510 to 525 m in order to pass." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2630m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Continued RIH with EVO plug. Lost CCL signal at 2630 m." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2630m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: Troubleshot and found short in downhole circuit." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 472m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: POOH with BHA #2 to 472 m." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: POOH from 472 m to surface." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.5 hours. Operational details: OOH. SIWHP 102 bar. Closed well and bled off pressure. Inflow tested HMV. Flushed riser/lubricator with N2. LD BHA #2." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 3.5 hours. Operational details: RU backup tractor and plug. Plug from BHA #2 was slightly gassed up and too large to be run. Stabbed on and leak tested QTS to 170 bar. Equalized across SV and HMV with MEG and opened well. SIWHP 102 bar." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2980m. The activity was categorized as 'interruption -- other' and lasted for 2.2 hours. Operational details: RIH with BHA #3, 7' EVO plug on tractor to 2980 m MDRKB. Had to work BHA through Baker AVLDM tubing hanger at 510 m." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3030m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Activated tractor and RIH from 2980 to 3030 m." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3265m. The activity was categorized as 'workover -- wire line' and lasted for 2.2 hours. Operational details: Performed correlation passes. Set EVO plug with pkg. element at 3274,8 m and top plug at 3274,25 m." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: POOH with BHA #3." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 3.0 hours. Operational details: Closed well. WHP = 99 bar. Held toolbox meeting on drill floor. Inflow tested HMV. Bled off and flushed lubricator with N2. LD and checked toolstring." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wait' and lasted for 0.8 hours. Operational details: Time out meeting in PCR with focus on communication." "On 2010-09-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Held SJA meeting on drill floor regarding RD. Closed DHSV and bled down pressure above to 63 bar through flowline to test sep. Meanwhile LD lubricator onto HTS." "On 2010-09-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.2 hours. Operational details: Bled down pressure above DHSV from 63 to 10 bar through flowline to test sep. Inflow tested DHSV." "On 2010-09-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Bled off pressure above DHSV and closed HMV. Opened BOP." "On 2010-09-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 1.5 hours. Operational details: Held toolbox meeting regarding RD WL equipment. Mærsk prod. dep. activated isolation plan, on all valves on wellhead." "On 2010-09-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Used top drive and lifted upper riser to drill floor. Rigged away WL BOP. Lifted lower riser by use of two tuggers." "On 2010-09-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 0.8 hours. Operational details: Removed Chiksan equipment on KWV and installed end cap. Installed x-mas tree top cap. Leak tested x-mas tree cross to 20 bar for 5 min." "On 2010-09-20, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- rig up/down' and lasted for 2.5 hours. Operational details: Leak tested x-mas tree cross. 170 bar for 10 min. Leak tested KWV end cap and XMT top cap to 20/345 bar for 5/10 min. Handed well over to Production Department. ______________________END OF OPERATION______________________" "On 2012-01-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Received and spotted equipment in work area." "On 2012-01-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Held prejob meeting with all involved personnel." "On 2012-01-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Spotted equipment in work area. Hooked up winch to power and F&G." "On 2012-01-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Spotted equipment in work area. Hooked up WellTec logging container to power and F&G. Prepared for testing of BOP." "On 2012-01-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held brief prior to testing of WL BOP." "On 2012-01-27, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.0 hours. Operational details: Leak and function tested BOP to 20/180 bar for 5/10 min. Meanwhile pulled out all cables and hoses needed." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Completed BOP testing." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Held prejob meeting with all involved personnel." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.2 hours. Operational details: Held brief regarding building of upper riser and lubricator. No crane driver on night shift due to cancelled helikopter." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.4 hours. Operational details: Built riser and lubricator on main deck. Used fork lift to assemble sections." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.3 hours. Operational details: Built GIH for 5/16' mono conductor cable." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.5 hours. Operational details: Completed GIH." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Held platform muster drill. Everybody attended." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.5 hours. Operational details: Hoisted down BOP into moonpool area through hatch on drill floor. Lifted up upper/lower riser, lubricator and grease head from main deck to drill floor. Completed assembling of riser/lub. Found that 5/16'cable drum chain was broken. Disassembled chain and ordered spares from shore with helicopter." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.5 hours. Operational details: Prepared miscellaneous hoses prior to rig-up. WellTec built new cable head. Meanwhile Halliburton checked DPU's." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: Held platform muster drill. Everybody attended." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: WellTec tested counter system. Meanwhile AWS repaired chain on 5/16'cable drum." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.5 hours. Operational details: Connected cables to winch BOP screen and smart skid. Secured hoses/cables over sharp edges. Checked chiksan at wellhead. WellTec checked tractors. Meanwhile Mærsk electrician repaired faulty hydr. sensor om WL winch." "On 2012-01-28, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Flushed DHSV hose and filled pump tank with hydr. oil from platform. Filled MEG on test pump. Started wireline winch OK." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Installed cover over drop-in-drum. Calibrated counters and pulled out 5/16' cable to test BHA." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.8 hours. Operational details: Connected cable to BHA and tested tractors and DPU setting tools." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 2.4 hours. Operational details: Closed in well to prepare for handover. Meanwhile: Tided area and completed check lists." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 4.2 hours. Operational details: Waited for Production Department to prepare well for handover." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.8 hours. Operational details: Took over well and leak tested XMT cross to 20/200 bar. Took off XMT cap and installed X-over/lower riser. RU BOP and function tested same. Leak tested connections against SV." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 1.0 hours. Operational details: Lifted down upper riser and connected to BOP. RU lubricator and upper sheave wheel in elevator." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.0 hours. Operational details: Installed BHA #1, EV0 plug and 3 1/8' tractor, into lubricator in three parts. Pumped MEG through production chemical line to fill lubricator and leak tested lubricator and QTS 5/10 min to 20/170 bar with AWS PT pump." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Opened HMV and pump MEG through production chemical line to equalize across DHSV and opened DHSV." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 0.5 hours. Operational details: Equalized and opened SV 44 turn." "On 2012-01-29, at Well NO 15/9-F-14, a drilling event occurred at a depth of 510m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: Opened well and RIH with BHA#1 EV0 plug. Lost some weight, indicating small restriction." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2945m. The activity was categorized as 'workover -- other' and lasted for 0.8 hours. Operational details: Continued RIH with BHA#1 to set EV0 plug. BHA stopped due to deviation/friction." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3140m. The activity was categorized as 'workover -- wire line' and lasted for 0.3 hours. Operational details: Started tractor and continued RIH to 3140 meter." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3140m. The activity was categorized as 'workover -- other' and lasted for 2.0 hours. Operational details: Performed correlation passes with CCL. Pulled up to CCL setting depth." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 3041m. The activity was categorized as 'workover -- other' and lasted for 0.3 hours. Operational details: Set EV0 plug and lost 500 lbs. Mid element set at 3040 m and top plug at 3039,22 m." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 2.5 hours. Operational details: POOH to surface with BHA #1." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- other' and lasted for 3.5 hours. Operational details: OOH. Closed well and bled off pressure. Flushed with N2 and inflow tested SV and HMV. L/D BHA #1 and verfied plug setting OK." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- test scsssv' and lasted for 1.5 hours. Operational details: Closed upper BOP ram, bled off above DHSV and inflow tested same. Meanwhile held brief and LD lubricator and sheave wheels on rig floor." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 5.5 hours. Operational details: Disconnected upper riser from BOP and LD same on rig floor. RD BOP and lower riser. Installed XMT cap and weco cap on TKV. Leak tested both to 20/345 bar for 5/10 min. Leak tested XMT cross to 20/170 bar for 5/10 min. Handed well over to production." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 2.8 hours. Operational details: Packed WL equipment for backload. Meanwhile Production Department flowed well to verify water shut off from plug setting." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 0.4 hours. Operational details: Performed Pre-job Meeting prior to rig down last items and clean area." "On 2012-01-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 4.3 hours. Operational details: Packed WL equipment for backload. Meanwhile Production Department flowed well to verify water shut off from plug setting." "On 2012-01-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'workover -- wire line' and lasted for 3.0 hours. Operational details: Prepared all equipment for backload. Cleaned and tidied work area. -------------------------------------------END OF OPERATION----------------------------------------------------------" "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.2 hours. Operational details: Completed checklists and permits for skidding operations. Prepared cantilever for skidding" "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding rig to F-14" "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Removed access stairs and bridge between produciton unit and cantilever" "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.0 hours. Operational details: Skidded rig to F-14" "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with ongoing crew for pulling hatch on F-14" "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Prepared to pull hatch. Lowered halv moon hatch on position. Meanwhile: Built scaffolding around XT." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Continued building scaffolding around XT. Meanwhile: Continued preparing for pulling hatch." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Pulled hatch on well F-14. Installed half moon hatch." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Lifted cement spool onto XT and M/U bolts. Installed hole covers in moonpool. Built scaffiling to access cement spool valves. Installed gauge and bleed off line on top of cement spool. Meanwhile: Performed maintenance on BOP and drilling equipment." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared moonpool. Meanwhile: Topped up A - and B annulus with SW." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing cement spool and lines." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Confirmed line-ups and valve positions, walked the lines. Prepared cement unit for pressure test. Meanwhile: Barriered off areas prior to pressure testing." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Applied 20 bar against closed LTV15, opened LTV15 and confirmed correct line-up." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Flushed cement spool. Pressure tested cement spool to 20/310 bar for 5/10 min. Bled off pressure." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Performed TBT for line-up and bullheading operations." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lined-up rig pumps and confirmed line-up. Opened HMV and SV. Pressurized DHSV control line to 520 bar." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Pressured up well to equalize DHSV by pumping 3m3 50/50 MEG/SW. Pumped 3,8m3 wash pill. Stopped pumping due to indications of DHSV not opening." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Investigated issue with DHSV. Kept 520 bar on DHSV control line and bled of pressure from well through closed drain. Monitored pressure on DHPG and observed pressure dropping 1 bar / 10 min while bleeding off well. Closed bleed-off valve and observed DHPG pressure increase, indicating that DHSV was in open position." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Staged up rig pumps to 1300lpm/71bar and bullheaded remaining 6,2m3 of wash pill followed by 208 m3 SW. Meanwhile: Performed TBT for cement job. After bullheading 118 m3 of SW the pressure increased from 71 bar to 91 bar rapidly. Continued bullheading SW at 1300lpm, pressure stabilized at 90 bar with a slightly decreasing trend. After bullheading 208 m3 of SW the pressure increased again from 90 bar to 100 bar rapidly. Pressure stabilized with steady trend at 100 bar." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued bullheading SW at 1300 lpm / 100 bar. Meanwhile: Mixed cement." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lined up and released bottom dart. Mixed and pumped 6,6 m3 1,90sg cement slurry at 600 lpm." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Displaced surface lines with 0,9 m3 hi-vis pill from cement unit. Released top dart and continued to bullhead 6,9 m3 hi-vis with cement unit." "On 2016-07-30, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Displaced cement with 41,5 m3 SW from cement unit at 1300 lpm / 85 bar, cycled DHSV 3x after bullheading 30 m3 of SW (while still pumping at 1300lpm). Continued displacement by pumping 3 m3 contamination pill at 600lpm / 56 bar with cement unit. After bullheading 2,7 m3 contamination pill the formation started to pack off, pressure increased from 56 bar to a final squeeze pressure of 95 bar. Stopped pumping, final static pressure 57 bar. Estimated TOC 2700 mMD." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: WOC. Closed SV and bled off pressure on cement unit and surface lines. Monitored pressure in XT cross from prod. control room. Meanwhile: Flushed lines from cement unit. Performed maintenance on BOP. Prepared to change out wires on FWD PRS. Bled off pressure in XT cross from 100 bar to 55 bar at 02:00." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: WOC Continued performing maintenance on BOP and FWD PRS. Bled off pressure in XT cross from 100 bar to 56 bar at 03:45 Bled off pressure in XT cross from 100 bar to 54 bar at 06:10" "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 5.0 hours. Operational details: WOC Continued maintenance on BOP and FWD PRS. Tested kill manifold to 20/310bar for 5/10min. Bled off pressure in XT cross from 97 bar to 55 bar at 10:40." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing and inflow testing cement plug" "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Closed HMV and bled off pressure between HMV and SV to closed drain. Opened SV and equalized above HMV. Opened HMV and pressure tested cement plug to 300bar / 10min. Volume pumped 560 ltrs from 67 bar to 300 bar. Monitored pressure from production control room." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Bled off pressure on well from 300 bar to 10 bar via closed drain." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: Performed 23 bar inflow test of cement plug for 20 min. Monitored pressure from production control room. Observed increasing trend. Pressure increased from 10 bar to 18 bar in 45 min (1,7 bar/10min), slightly flattening. Consulted town, agreed to continue inflow testing. Bled off pressure in well from 18 bar to 10 bar via closed drain. Performed new inflow test of cement plug. Pressure increased from 10 to 20 bar in 1,5 hrs (1,1 bar/10min), slightly flattening. Meanwhile: Pressure tested BOP. Continued maintenance on FWD PRS." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.0 hours. Operational details: Performed new inflow test of cement plug for 3 hrs. Pressure increased from 10 bar to 27bar (0,95 bar/10min). Meanwhile: Continued pressure testing BOP." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Bled down pressure in well to 10 bar and performed new inflow test of cement plug. Monitored pressure for 30 min. Pressure increased 0,7 bar / 10min, flattening trend." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Finished ongoing BOP test." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Pressured up well to 310 bar with cement unit. Pumped 715 ltrs from 13 bar to 310 bar. Bled off pressure in DHSV control line. Bled off pressure in well to 240 bar. DHPG indicated DHSV in closed position. Performed 70 bar low-pressure inflow test of DHSV for 30 min." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Bled down pressure in well to 10 bar. Performed 300 bar hi-pressure inflow test of DHSV for 30min." "On 2016-07-31, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pressured up well to 310 bar with cement unit, pumped 207 ltr from 12 bar to 310 bar. Observed DHSV opened at ~288 bar (after 150ltrs pumped). Applied 520 bar pressure on DHSV control line. Bled off well to 20 bar through closed drain. Bled off pressure in DHSV control line." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Closed swab valve and continued bleeding off remaining pressure in well back to cement unit. Read 274 bar on DHPG, indicating DHSV in closed position." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Rigged up lifting arrangement to lift off cement spool" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Released connection between XT and cement spool. Lifted cement spool off of XT and landed cement spool in moonpool." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: P/U BPV plug from HTS. RIH and installed BPV plug in TH. Meanwhile: Pressure tested BOP." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Installed lifting cap on XT. R/D and removed production flange from XT. Meanwhile: Pressured up ASV control line to 520 bar, no pressure increase on A-annulus observed. Pressure tested BOP." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT with new ongoing crew" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D chicksan and piping from XT" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed instrumentation on XT and R/D scaffolding" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled split hatch. Pulled hatch on nabour well and R/D support beam. Built scaffolding (fence) around open hatches." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for lifting XT" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U lifting arrachement on TDS" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lifted XT from XT-deck to moonpool. Meanwhile: Pulled foxhole" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Load transfered XT from TDS to moonpool gantry crane. Moved XT into moonpool and landed on skid. Secured XT on skid. Meanwhile: Prepared to lift spool piece from WH." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed master bushing and hole cover." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Verified no pressure in TH void ports. Removed hatck on XT-deck. Meanwhile: Installed foxhole." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed master bushing and lowered lifting arrangement from TDS. Attached lifting arrangement to spacer spool. Lifted spacer spool from WH to drill floor and L/D same." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed support beam and hatches. Installed split hatch on F-14. Installed master bushing and hole cover." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 3.2 hours. Operational details: Cut control lines in multibowl. Prepared to install communication collar. Installed dart in BPV plug" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Installed communication collar. Meanwhile: Pressure tested BOP." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U surface hi-pressure riser. Attached lifting arrangement to TDS, using double securing." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed hatch cover in moonpool. Removed master bushing. Installed scaffolding (fence) around rotary." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lowered surface hi-pressure riser onto multibowl." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Built scaffold around BOP test stump. Meanwhile: Prepared BOP for moving to well center." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Disconnected NT2 connector on test stump and removed test mandrel from BOP." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lifted BOP from test stump and moved BOP approximately 1m towards well center." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for inspecting NT2 connector" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Inspected NT2 connector. Meanwhile: Built scaffolding around HP riser in moonpool. Cleaned and cleared moonpool. Removed flange from kill wing on XT." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for skidding BOP" "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Skidded BOP over well center. Installed seal ring. Landed BOP on connector." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed slick joint." "On 2016-08-01, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Installed master bushing. Lifted diverter with TDS. Removed master bushing and lowered diverter." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Landed diverter." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 4.2 hours. Operational details: R/D lifting equipment. Installed master bushing. M/U slick joint and installed tension cylinders. Meanwhile: Performed maintenance on drilling equipment." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Filled BOP and riser. Attempted to perform connector test to 310bar/10min. Pressure started to drop at 296 bar, stopped pumping. Trip tank steady during testing. Performed line test to 310bar/10min against kill valve on BOP, no leakages observed." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Evaluated situation. Meanwhile: Performed housekeeping on drill floor." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Prepared to retrieve BPV dart and plug. Lifted equipment to drill floor." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for retrieving BPV dart and plug." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: P/U retrieval tool." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Attempted to M/U 3 1/2' DP. Changed dies carrier in AFT IRN." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RIH with dart retrieval tool to 19,7m. Made 3 attemptes. Released and retrieved dart." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: RIH with BPV retrieval tool to 19,9m. Retrieved BPV plug to surface." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Inspected BPV, no signs of damage. P/U new BPV plug and dart. RIH to 19,1m and installed BPV plug. POOH. RIH to 19,3m with dart and installed same. POOH." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for new connector test." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed line-up test to 20 bar." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Performed connection test to 20bar/310bar for 5/10min. Volume pumped from 20 bar to 310 bar, 60 ltrs. Bled back same." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: RIH and retrieved dart and BPV plug. POOH." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: B/O and L/O retrieval tool." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U to pressure test TDS" "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: M/U pump-in sub to TDS and connected cement hose." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pressure testing TDS." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Pressure tested lower and upper IBOP, Kelly hose and S12 valve to 310bar/10min. R/D pump-in sub and cement hose." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Prepared hoses and equipment for THRT. Meanwhile: Installed lifting tool in FWD PRS. Tightened fittings on FWD PRS." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: R/U casing handling equipment, dressed for 7'." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with THRT and landing string." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U and M/U tubing hanger running tool. M/U and RIH with landing string. POOH. M/U control lines and flushed same." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Lined-up to pressure test kill manifold." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Pressure tested kill manifold (body test) 20/345bar for 5/10min." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH with THRT to 21m and landed on TH. Orientated J-slot 90 deg. Took 2 ton overpull. Applied 14 - 21 bar on tool, string dropped approx. 2'. Engaged communication collar by turning string 8 turns LH." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Rigged up hose on A-annulus wing on multibowl. Meanwhile: Changed elevator." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for installing swedge and open DHSV" "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Changed fittings on hose for elevator due to leakage." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Inspected swedge and found mark on seal face. Filed sealface. M/U swedge on 7' landing string." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed cement hose and lo-torque valve. Pressure same to 100bar." "On 2016-08-02, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Applied 520 bar on DHSV control line. Pressured up tubing with rig pumps. DHSV opened at 75 bar. Bled down pressure through mud-gas separator. Monitored for pressure build up for 5 min." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Applied 420 bar on ASV control line. Pressured up A-annulus to 50 bar from cement unit. Pumped 16ltrs from 10 bar to 50 bar, ASV not open. Closed lo-torque valve on A-annulus wing on multibowl. Pressured up lines to 20 bar and opened lo-torque valve, no pressure drop observed. Troubleshot A-annulus valve on multibowl, both A-annulus valves in open position." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Re-attempted to pressure up A-annulus to 50 bar from cement unit. Pumped 18ltrs from 10 bar to 50 bar. No indication of ASV opening. Performed new line-up test and checked all valves." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Attempted to increase A-annulus pressure in stages of 10 bar to 120 bar with control line pressure of 480 bar. No indications of ASV opening. Pressure leaked off 1,5 bar/min. Bled off pressure. Volume pumped to 120 bar, 23ltrs. Bled back same." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Pressured up A-annulus to 120 bar, then applied 480 bar pressure on control line. No indication of ASV opening. Pressure leaked off 1,5bar/min. Bled off control line and A-annulus. Volume pumped 23 ltrs. Bled back same. Performed line-up test to 120 bar, opened lo-torque valve. No pressure drop seen when opening lo-torque. Checked all valves and hoses. R/D hose on A-annulus wing and observed cement residues coming out from hose. Replaced hose." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Pressured up ASV control line to 420 bar. Pressured up A-annulus from cement unit to 50 bar. Pumped 136 ltrs from 10 bar to 50 bar (expected volume to pump 82 ltrs). Possible air/gas. Bled off pressure through mud-gas separator. Pressured up A-annulus again to 50 bar while applying 420 bar on ASV control line. Pumped 129 ltrs from 10 bar to 50 bar. Bled down pressure through mud-gas separator." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D cement hose and 7' swadge." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U WL" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U wireline equipment." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for handling explosives and P/U toolstring" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: M/U cutter toolstring. Armed the cutter." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 520m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: RIH w/ cutter toolstring from surface to 520 mMD" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 506m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Correlated. Positioned cutter at 505,6 m. Performed cut. Indications of positive cut, heard shot at surface." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 70m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH from 505,6 m to 70 m . Average pulling speed 30 m/min." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 70m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for L/D toolstring" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D WL toolstring" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/D wireline equipment." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling TH and tubing" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/U C/L spool and built scaffold shelter for operator. Prepared slips." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 489m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released and pulled TH, 25 ton overpull. Pulled hanger to surface and disconnected control lines from THRT." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 489m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH again with landing string. POOH and L/D landing string." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 489m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Cut control lines. Blinded off chemical injection line. Rigged up spooling unit. Installed FMS slips." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 489m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/D down tubing hanger and running tool" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 477m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: POOH with 7' tubing from 489 mMD to 477 mMD." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 477m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Spooling unit not equipped with break. Attached carabiner to avoid spooling out control line when setting slips." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 465m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: POOH with 7' tubing from 477 mMD to 465 mMD. Adjusted slips alignment to avoid clamps haning up on slips while POOH. Rigged up remote control panel outside driller's cabin." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 237m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: POOH with 7' tubing from 465 mMD to 237 mMD. Average pulling speed 6,8 jnt/hr." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 237m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pulling tubing with ongoing crew" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 8m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: POOH with 7' tubing from 237 mMD to 8 mMD. Average pulling speed 7,5 jnt/hr." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cut control lines and secured same on spool. L/O DHSV. Marked DHSV. Measured length from top box down to cut 10,97 m." "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: R/D casing handling equipment. Meanwhile: Changed inserts in elevator. Installed PS-21 slips" "On 2016-08-03, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U and M/U cutter BHA. Inspected and set slips. M/U XO for surface test of cutters." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: M/U XO with wrong threads (NC38 Vam Eis - DS38). B/O XO and observed damage on XO. Changed inserts in elevator and P/U single w/ XO from cantilever. M/U same to BHA." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Lined up for testing cutter" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: M/U TDS and tested cutter in rotary. Knives opened at 170 lpm/ 12,5 bar. Secured knives and B/O TDS." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: B/O XO and single. L/D same" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 12m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH with cutter BHA from surface to 12 mMD. Installed PS-21 slips." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 282m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: RIH w/ cutter BHA on 3 1/2' DP from 12 m to 282 m. Avg. tripping speed 180 m/hr. Re-arranged 3 1/2' HWDP in set-back in order to access 3 1/2' DP." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 282m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Changed to 5 1/2' handling equipment" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 363m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH w/ cutter BHA on 5 1/2' DP from 282 m to 363 m." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 363m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Function tested BOP" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 722m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Continued RIH w/ cutter BHA on 5 1/2' DP from 363 m to 722 m. Average tripping speed 360 m/hr. Entered 7' cut carefully at 505,6 m." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 736m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: M/U TDS and filled pipe 500 lpm." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 754m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: Recorded paramters: 80 rpm/1-4 kNm; 100 rpm/1-4 kNm Up/down weight 82/80 ton 200 lpm/58 bar Positioned cutter at 754,3 mMD and cut tubing. Observed clear indication of cut, pressure dropped." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 754m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Lined up on TT and flowchecked well for 10 min, initial loss rate 600 ltr/min. Lost for 7 to 8 min, then static. Meanwhile: Performed TBT for POOH" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 684m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: POOH wet w/ cutter BHA from 754 mMD to 684 mMD." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 684m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: R/U mud bucket" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 280m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Continued POOH wet w/ cutter BHA on 5 1/2' DP from 684 m to 280 m . Avg. tripping speed 800 m/hr." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 280m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: B/O and L/D 3 1/2' x 5 1/2' XO Changed to 3 1/2' handling equipment." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH w/ cutter BHA on 3 1/2' DP from 280 m to surface . Avg. tripping speed 270 m/hr." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: L/D cutter BHA to HTS" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U FLX cutter BHA assy #1 from cantilever Meanwhile: Performed TBT for M/U and RIH with BHA" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Changed inserts in elevator to 5 1/2'." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 16m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U and M/U FLX cutter BHA assy #2. L/D 2 ea 3 1/2' pups." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 499m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: RIH w/ FLX cutter BHA on 5 1/2' DP from 16 m to 499 m. Avg. tripping speed 386 m/hr." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 517m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Tagged no-go at 517 mMD with 2 ton. Verified pipe count and marked pipe." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 517m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: M/U TDS. Filled pipe at 500lpm, reduced rate to 250 lpm before full pipe." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 516m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Recorded parameters: up/down weight 83/79 ton; free rot. torque 1 - 7kNm; 200 lpm / 53 bar, 250 lpm / 90 bar. Spaced out and placed cutter at 514,8 mMD. Cut FLX inner mandrel at 514,8 mMD, observed pressure drop. Stopped rotation and set down 2 ton. Pulled up 6cm and observed pressure increase." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 338m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Lined up to TT. POOH wet w/ cutter BHA on 5 1/2' DP from 516 m to 338 m. Avg. tripping speed 712 m/hr." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 338m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed kick drill" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 16m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: POOH wet w/ cutter BHA on 5 1/2' DP from 338 m to 16 m. Avg. tripping speed 644 m/hr." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Inspected cutter and L/D BHA." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Serviced and greased TDS." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Changed inserts in elevator. Retrieved spear assy from fingerboard." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for RIH with spear BHA" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U spear BHA. Inspected grapple and greased helix." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 41m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: P/U and M/U single" "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 498m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: RIH w/ spear BHA on 5 1/2' DP from 41 m to 498 m . Avg. tripping speed 610 m/hr." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 511m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: M/U TDS and took up/down weights 82/74 ton. Engaged fish. Worked string up/down several times with max 22 ton OP/WOB. Pulled FLX free with 23 ton OP. Pulled up 3 m and waited 30 min for elements to retract." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 58m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: POOH w/ spear BHA and FLX/tubing on 5 1/2' DP from 508 m to 58 m . Avg. tripping speed 360 m/hr." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 43m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: L/D 5 1/2' DP single." "On 2016-08-04, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with fish and set slips on tubing. Removed clamps and released spear." "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Inspected and greased grapple. R/B spear BHA." "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 249m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/U csg handling equipment." "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 249m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U handling equipment for pulling 7' tubing. Installed spooler unit." "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 236m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled out with ASV/FLX assy. Installed FMS slips. L/D ASV/FLX and pup joint. Performed LRA readings." "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.8 hours. Operational details: POOH with 7' tubing from 236 to surface. Average pulling speed 8 jnts/hr. Performed LRA readings every 5th joint." "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed FMS slips and installed master bushing R/D casing tong." "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 41m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U spear BHA (run#13), RIH to 41m" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 754m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: RIH w/ spear BHA (run#13) on 5,5in DP from 41 m to 754m. RIH speed 475m/h" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 754m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Recorded weights up-92t, down-86t" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 754m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Engaged spear, pulled tubing free at 168t hook weight. No indication of pins shearing noticed when tubing went free" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 754m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: Observed backflow from the tubing. Pulled one stand and monitored backflow. No change" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 81m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Continued to POOH wet from 754m to 81m" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 81m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Flowchecked well for 15 min. Stable" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 41m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: POOH w/ fish from 81m to 41 m. Meanwhile held TBT for rigging up casing tongs" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Installed casgin tongs over well center, changed PS21 slips to master bushing" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to release spear from the fish" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released spear and inspected grapple. Grapple in good condition. R/B spear BHA (run#13) in derrick" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Broke off cut. Observed high torque. Changed elevator inserts and pulled out 1x single, removed clamp and L/D same" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Cleaned and inspected swage before M/U" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: M/U swage. Overtorqued connection due to wrong setting on casing tongs. Broke off swedge and inspected connection. Performed TBT prior to pull out overtorqued box" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: POOH w/ tubing with overtorqued box, arranged double securing to box. Set slips, removed double securing to box. Removed clamp and broke off single, L/D same" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Inspected box treads. P/U backup 7in pup w/ expandable plug. Alligned pup over stump, made up 2x turns with chain tong, removed elevators and M/U connection w/ casing tong" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: M/U swedge to 7in tubing" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: R/D casing tong" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: M/U stand of 5.5in DP to swedge. Changed out master bushing to PS21 slips" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2541m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 2.2 hours. Operational details: RIH w/ 7in tubing on 5,5in DP from 1816m to 2541m . Filled pipe every 250m" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2578m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: M/U TDS, RIH to 2578m" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for cement operation" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Installed cement stand, M/U TDS again, installed cement hose. End of tubing is at 2581m before started pumping" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Circulated 45m3 of SW at 3000lpm/89bar. When 40m3 pumped pulled string to 2580m. 0.3% HC gas observed in returns. Circulated additional 10m3 of SW. Totally circulated 55m3 of SW. Pumped 20m3 of wash pill at 2700lpm/76bar" "On 2016-08-05, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pressure tested last line connection to pump in sub to 310bar for 3 min. Good test. Bled off pressure to 20bar. Opened LTV and confirmed line up." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2580m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Balanced cement plug (2330 m - 2580 m ): Mixed and pumped 9,2 m3 of 1,9 SG cement slurry, 630 l/min. Displaced the cement to the rig floor with 2900 l of drill water. Zeroed volume counters. Displaced the cement with 30,7 m3 (1386 strokes) of SW, 2000 l/min/ 3 bar." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2295m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: Pulled out of cement to 2295 m MD. Theoretical TOC 2330 m MD." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2287m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Installed sponge ball, M/U TDS, pulled to 2287m. Pumped 10m3 of hi-vis pill. Circulated total of 74m3 at 2700lpm-38bar until clear returns observed." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2219m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH from 2287m to 2219m." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2219m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.5 hours. Operational details: Installed BOP jetting tool, washed BOP cavitied with 1450lpm, 8bar, made 5 passes. Function tested BOP and washed another 5 passes." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1843m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: POOH from 2215m to 1843m." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1843m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Removed PS21 slips and R/U casing pulling equipment" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1843m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for pulling tubing" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1843m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Broke swage, R/B stand of drill pipe and changed BX elevator inserts" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1366m. The activity was categorized as 'plug abandon -- other' and lasted for 5.2 hours. Operational details: POOH with 7in tubing from 1816m to 1366m (38 joints or 450m of tubing), removed clamps and spooled control line. Average pulling speed 7.2 joints/hour, max pulling speed 10 joints/hour. Cut control line and secured to tubing with clamp on the last joint. Observed fluid spraying out of control line" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1366m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for engaging spear and R/D casing pulling equipment. Observed fluid spraying out of control line" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1366m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Crimped control line to stop fluid spraying out. Removed spooler and scaffold shelter from setback area" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1366m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U spear and engaged in 7in tubing. RIH w/ spear below rotary to change slips" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1366m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/D casing equipment and installed PS21 slips. Removed tong from frame in preparation for next operation. Meanwhile change BX elevators out for offline inspection and inspected and greased 10 3/4in grapple" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1366m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Serviced both PRSs" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1366m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Cleared rig floor, meanwhile Installed inserts in BX elevators. Doped pipe in derrick" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2278m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: RIH w/ tubing on spear to 2278m. Avg. tripping speed 680 m/hr." "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2359m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: Washed down from 2247m to 2320m with 560l/min and 6 bar. Did not find hard cement. Decreased flow to 222lt/min 1.2bar and continued to wash down to 2359m" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2335m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.2 hours. Operational details: POOH from 2359m to 2335m and circulated bottom up with 1350l/min 53bar and then increased to 2020l/min 109bar. In the end of circulation some loose cement was observed in the shakers along with consolidated clumps of cement. Otherwise mostly clean fluid in returns. Meanwhile recalculated BHA figures after discrepancy was found" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2420m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.0 hours. Operational details: Washed down from 2335m to 2420m with 560l/min 7,4 bar. Did not encounter hard cemtent. 60m left to go before hitting minimum length of plug (at 2480m). When making connections observed back flow from DP indicating heavier fluid in annulus" "On 2016-08-06, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2398m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH from 2420m to 2398m and circulated BTM up with 2020 l/min, 106bar. Reduced flow just before BTM up due to possible cement in returns. After BTM up , increased flow to 2660 l/min and 180bar and continued to circulate. Observed some loose cement in returns on shakers." "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2398m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Evaluated situation. Discussed situation w/ cementing support onshore organisation. 24 hours WOC by now. Agreed to continue attempting to tag cement" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 2456m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: Continued to wash down from 2398m with 560l/min 20-25bar, observed pressure spikes up to 85 bar. Tagged hard cement at 2456,5m with 12t, 530l/min, 22bar. Length of cement plug 123,5m (2456,5m - 2580m)" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 1096m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Released spear from tubing: set down 30ton, 2x turns right, pull up 200m to confirm free. Top of tubing in the well at 1096,5m" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 1.5 hours. Operational details: POOH w/ spear BHA (run#16) on 5,5in DP to surface. Average pulling speed 703m/hour" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH w/ spear BHA (run#16), inspected and R/B same" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed PS 21 and installed master bushing" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting for retrieve MS-T surface seal assy" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U MS-T seal retrieving tool. M/U to stand and function tested tool" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ MS-T seal retrieving tool. Landed of at 20, 5m" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed pre-job meeting for retrieve MS-T surface seal assy w/ new crew" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Attempted to engage tool by rotating 5 turns to the left with chain tongs. No go" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 21m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Discussed forward plan, removed double from stand above retrieval tool, picked up 1.5m pup and 3m pup" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Attempted to engage tool by rotating 5 turns to the left using chain tongs. Only able to get Approx. 1 ¼ turns" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Rotated tool out and retrieved to surface, inspected same. Marks observed on the outside of the tool" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Evaluated situation" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: P/U wash tool, M/U to FOSV then to double and measured in hole. Jetted BOP 1500 l/min, 8.7 Bar, 5 RPM, TQ 0-1 KNM. Function tested BOP" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Continued to jet BOP after function test. 1500 l/min, 8.7 Bar, 5 RPM, TQ 0-1 KNM" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: B/O TDS and measured in to top of well head, M/U to TDS and jetted wellhead seal area 1500 l/min, 8.7 Bar, 5 RPM, TQ 0-1 KNM" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH with wash tool and lay out same" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Repaired elevator leak. Replaced valve on same" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Transfered MS-T seal retrieval tool to TDS and re-positioned hose spools" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: RIH with retrieval tool and attempted to engage tool by rotating 5 turns to the left. Approx. 3,5 - 3,75 turns" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released tool and POOH, inspected same. Marks observed on the outside of the tool" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.2 hours. Operational details: Contacted wellhead support organization regarding forward plan for pulling the MS-T seal. Meanwhile inspect TDS, covered electrical equipment on drill floor in preparation for deluge test. Performed deluge test on rig floor. Crane operator moved equipment to rig floor due to high wind forecast in preparation for next ops. Re-arranged link tilt arms on TDS" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH and engaged by rotating the retrieval tool 3,75 turns to the left. Connected hose to pump and energize lock ring and bled off pressure. Then pressured up MS-T seal. M/U TDS and retrieved MS-T seal w/ 87T overpull observed. POOH with MS-T seal" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Released seal assembly from tool. L/D retrieval tool" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 0.5 hours. Operational details: WOW due to high winds (48knot) for crane operations. Meanwhile serviced drilling equipment and performed housekeeping. Prepared work permits for crane work in high winds" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: P/U cutter assembly and inspected same (BHA#18)" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: M/U to 5,5in DP stand and TDS and RIH to position cutters at 23.6m , recorded drilling parameters 300l/min - 29bar, 500l/min - 90bar, 70t up / 65t down" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cut 10 3/4in surface tie back at 23,6m with 300l/m and 80 rpm 2 - 12 torque. Good sound indication of successful cut heard on surface" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: POOH with cutter (BHA#18) from 23.6m, inspect knives, L/D BHA" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U and M/U w/ ITCO spear (BHA#19). RIH, took up/down weights: 70t up/67t down. Engaged fish" "On 2016-08-07, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released spear from fish and R/B same, L/D fish" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed prejob meeting to P/U torque tool" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U torque tool (BHA#20)" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: RIH w/ torque tool (BHA#20) to 135m. Washed down from 135m to 140,5m w/ 150lpm - 12 bar. Positioned tool at no-go (140,34m), applied torque gradually to 30 kNm and rotated 6 turns left to release adapter. Observed break in string" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Rotated 6 turns right to make up possibly broken connection in the string w/ torque limit of 5kNm. POOH and checked every connection. Discovered broken 5.5in DP connection below rotary table. Continued to POOH, checked all connections on the way out. Inspected torque tool." "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: RIH w/ torque tool on 5.5in DP. DP torqued to 52kNm. Repeated sequence to release tieback adapter. Observed string broke at 30kNm and rotated 6 turns left to release adapter. Rotated 6 turns right to make up possibly broken connection in the string w/ torque limit of 5kNm. POOH and checked every connection. Discovered broken 5.5in DP connection below rotary table. Continued to POOH, checked all connections on the way out. Inspected torque tool." "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: RIH w/ torque tool on5,5in HWDP. Connection torqued up to 67kNm. P/U last stand with overtorqued 5,5in DP and M/U connection to 57kNm. Attempted to release tieback adapter. Observed saver sub backing off at 30kNm" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Evaluated situation. Decided to make another attempt using rig tongs" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting for using rig tongs" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Attempted to release tieback adapter using rig tongs. Applied up to 40kNm, observed break in the string. Turned 4 turns left and measured, no noticable change. Screw string back 4 turns" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: POOH and checked every connection. Discovered broken 5.5in DP connection between HWDP and DP, M/U connection to 57kNm. Continued to POOH, checked all connections on the way out. Inspected torque tool" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Broke off torque tool and L/D same. Meanwhile discussed forward plan" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: P/U 10 3/4in casing cutter and RIH same" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to RIH w/ high wind and wind direction affecting running equipment" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: RIH w/ 10 3/4in csg cutter BHA to 87m. Stopped operation due to high wing causing the drag chains to twist laterally" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- waiting on weather' and lasted for 2.0 hours. Operational details: WOW. Meanwhile changed dies and dies holder in IR" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: RIH w/ 10 3/4in csg cutter BHA from 87m to 127m. M/U TDS, filled string, recorded parameters: 300 l/min - 27bar, 400l/min - 53bar, 500l/min - 84bar, up/down 73t/70t. RIH to 136m" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cut casing at 136m with 300l/min - 27,5bar - 80rpm - 2-10kNm. Observed pressure droped to14 bar. Increased slowly to 26,5bar. Increased rate to 400l/min - 45 bar. Confirmed cut by no rotation and 500l/min - 83bar. Lifted casing on knifes +/- 15cm w/ 8t overpull" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: POOH w/ cutter from 136m to surface. Meanwhile performed kick drill 31 sek. L/D cutter" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U spear BHA" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: RIH w/ spear to 34m. Took up/down weights 72t/68t" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Engaged fish w/ 1 turn left, pulled up to 82 ton on hook load" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: POOH with fish from 34m. Released spear. Closed annular with 270psi and pulled slowly out of fish. R/B spear. Meanwhile performed TBT for R/U casing equipment" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: R/U handling equipment for 10 3/4in csg" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull casing" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Broke out and L/D casing cut and pup" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Installed BX3 elevator w/ 10 3/4in inserts" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.5 hours. Operational details: POOH w/ 10 3/4in csg tieback from 136m to surface. Totally 10 joints pulled" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D csg tong" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: R/D csg tong" "On 2016-08-08, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: M/U torque tool and RIH on 3x stands of 5,5in HWDP and 1x stand overtorqued 5,5in DP. M/U all connections to 67kNm" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to use manual rig tong" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Attempted to release tieback adapter w/ manual tongs several times. Applied left hand torque in steps. Used TDS brake to lock in torque when making new bite with manual tong. Adapter came loose at 42kNm torque. Rotated string approximately 6 turns left, observed mark on pipe moved 3 inches up" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: POOH w/ torque tool, L/D same" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: P/U ITCO spear (BHA#24). RIH same on 5,5 DP to top of the fish at 136m. Engaged spear to fish." "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.8 hours. Operational details: POOH w/ fish from 136m to surface" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Set slips on 10 3/4in tieback casing stump. Released spear and R/B same. L/D tieback adapter fish" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to handle guns" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: M/U gun (BHA#25)" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to RIH w/ gun" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: RU to run gun. Changed handling equipment" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: RIH w/ gun (BHA#25) to 140m. Installed gog collar on all stands. P/U 3m pup" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: M/U TDS. Took up/down weights: 73t/69t, RIH to 148,5m bottom shot" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: Closed UPR, opened choke. Applied 10 bar on IBOP. Opened IBOP to confirm line up. Filled string. Opened UPR, Broke off TDS and droped 1 1/8 ball in string. M/U TDS. Closed UPR and opened choke. Fired guns with 130 L/m, 137 bar. Top shot at 145,5m, bottom shot at 148,5m Continued to circulate w/ 160l/min - 4,8 bar. Mud in returns" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: Increased pump rate to 1000l/min -7,6 bar. Pressure droped to 2,7 Bar. Observed only water in returns. Circulated 2x bottom up, max gas 0,1%. Stoped pumps. Observed H2S readings after 2 min. Continued to circulate w/ 1000l/min - 2,7 bar. Max H2S gas in return fluid 8ppm" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Flowchecked well over choke. Static" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Flowchecked well over trip tank. Static" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.8 hours. Operational details: L/D 3m pup. POOH w/ gun (BHA#25) from 148,5m to 14,4m" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 1.0 hours. Operational details: Broke off firing head, recovered blank, L/D BHA and single. All shots fired" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- perforate' and lasted for 0.2 hours. Operational details: Changed handling equipment" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U milling assy (BHA#26)" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.0 hours. Operational details: P/U cutter assy (BHA#21), broke off float sub, L/D cutter assy (BHA#21). M/U taper mill and hanger mill (BHA#26), changed handling equipment. P/U Shock tool and M/U to taper/hanger mill. Installed float sub, installed string magnet and x-over" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 2.5 hours. Operational details: P/U 9x 8,25in DC from cantilever and RIH. RIH to 135M w/ 1x stand of overtorqued 5,5in DP" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Carried out drop check on TDS. Serviced drilling equipment" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: P/U single. Recorded parameters: up/down weights - 86t/82t, 80 rpm, 2000l/min - 11bar. Tagged at 140,44m" "On 2016-08-09, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 4.0 hours. Operational details: Mill 10 3/4in subsea csg hanger. 1970l/min, 9bar, 80-120rpm, 5-13kNm, 1-8t WOB" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: Continued milling 10 3/4in subsea csg hanger. 1970l/min, 9bar, 80-120rpm, 5-13kNm, 1-8t WOB. Heard sound and observed loss of WOB indicating casing parted from hanger. Total of 27cm milled." "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Passed up/down several times through hanger area with and without rotation. Max 4t overpull without rotation. Tagged casing stump at 141,84m w/ 4t." "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.8 hours. Operational details: Dressed off top of casing from 141,84m to 141,91m (7cm). Parameters: 1970l/min, 80-120rpm, 5-13kNm, WOB 1-6t" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Circulated 2x BU 3000l/min - 23bar" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: L/D 1x DP single" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.5 hours. Operational details: Performed drops inspection and service on TDS. Observed loss in TT of +/- .8m3/hour. Inspected and confirmed no leak on surface" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.5 hours. Operational details: Continued monitoring well on TT while discussing way forward. Meanwhile TBT for POOH. Constant loss rate of 0,8m3/hour" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 1.0 hours. Operational details: POOH w/ milling BHA to surface. Losses decreased to +/- 0,4m3/hour while POOH" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.8 hours. Operational details: L/D milling BHA. Inspected magnet. Very fine swarf observed, not possible to weigh. Loss rate less than 0,1m3/hour" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mill' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to P/U cutting assembly" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.8 hours. Operational details: M/U cutting assembly" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Installed PS21" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: RIH with cutting assy from 16M on 5,5in DP to 767M" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 2.2 hours. Operational details: LD 1x DP single. M/U spear assy. Removed PS21, installed master bushing. Inspected and greased up spear. RIH 1x stand of DC" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: RIH from 821m to 900m on DP. Filled string. Up/down weights 106t/100t. RIH to 918.9m" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Pulled up to 170t on hook load (10 ton overpull) in order to engage spear inside 10 3/4in csg and put casing in tension Started cutting casing: 1700l/min - 92 bar, 1800l/min - 97 bar, 1900l/min - 101 bar, 2000l/min - 104 bar. Pulled up to 187t on hook load (25t overpull). Increased to 2200l/min - 124 bar. Casing cut at 915.2m" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Pulled up through 10 3/4 hanger with 10 3/4in casing, ok to pass. RIH back, released spear from 10 3/4in casing fish" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.2 hours. Operational details: Pulled free of fish, hung up with grapple at 139.4m through hanger. Troubleshoot to get through. Attempted to pull with max 10 ton overpull - no success. Pulled up slowly and rotate to the right - no success. Tried to rotate to the left and pull - no success. Pulled and pumped with 200l/min - 4 bar, pressure increased to 30bar when took weight at 139.4m. RIH and engaged spear inside 10 3/4in csg, pulled same through the hanger - ok. Rotated it 4.5 turns to the left (2-3k torq) to reposition casing fish inside the well. Landed fish in the well and released spear. Attempted to pull spear through hanger - no success. Pulled up total of 3,4m from top of csg stump at 141.9m" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.5 hours. Operational details: Evaluated situation. Discussed w/ onshore organisation. Meanwhile manufacturing c-plate to be able to hang off weight of the inner string Decided way forward: - pull csg fish on spear - release spear from fish - instal string stab above spear - engage spear on surface, RIH fish on spear - release spear, POOH" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull out fish on spear to surface" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.2 hours. Operational details: Engaged spear to fish. POOH fish slowly. Top of fish hang up in hanger area. Rotated string 180 deg left, pulled up. Went through When POOH observed overpull spikes on weight indicator several times. Max spike value of 40t" "On 2016-08-10, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: R/B 1x stand of DC, L/D bumper sub and string stab" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: Installed lifting sub, P/U string and set slips on casing. Released spear from fish. Inspected spear grapple. No signs of impact on grapple observed. Grapple in good condition" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: Installed C-plate and additional BX-elevator as false rotary on top of casing stump. Set of weight of string in BX-elevator and broke connection above. L/D Spear assembly on HTS" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to rearrange BHA" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.8 hours. Operational details: Rearanged spear BHA in foxhole to include 1x string stab (12in OD) above the spear grapple" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: P/U spear assembly and M/U to DP in well center Engaged spear to 10 3/4in csg fish" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH w/ 10 3/4in csg fish on spear. Released spear from the fish" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Attempted to pull spear several times. Max overpull of 10t, with and without torque. No success" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 3.2 hours. Operational details: Engaged fish on spear. Evaluated situation. Discussed way forward. Reviewed BHA/well schematic and concluded that it was not grapple that hung off, but taper mill hung off. Meanwhile cleared rig floor, serviced drilling equipment, removed scaffold from forward RPS" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 919m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: Released fish. Pulled gradually to 170t weight on hook (65t overpull). Observed drop on hook load to 103t indicating string free." "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 919m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH w/ BHA#27 on 5,5in DP from 910 m to 789m." "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 789m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.5 hours. Operational details: Removed Xover and pup above drill collar. Installed bumper sub. Inspected, cleaned and serviced grapple. Broke out Xover below spear and installed ball sub." "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 774m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: R/B spear assy, L/D pup joints, P/U single" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 774m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Installed PS 21" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 16m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH from 741m w/ cutter using mud bucked to 16m" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 16m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Removed PS 21 and installed master bushing" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: POOH w/ cutter assy. L/D same. Inspected cutter. Signes of wear on the knives. Piece of taper mill missing (size of 2-3cm)" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Cleared and cleaned rig floor" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 27m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: P/U and M/U spear BHA (run#28). Inspected and serviced grapple" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 108m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: RIH w/ spear assy from 27m to 108m" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 144m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U TDS. Up /down weights 75t/71t. RIH to 144m to engage fish. Took 5 ton over pull to confirm fish engaged Pulled to 130t on hook load. Casing free" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 771m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.5 hours. Operational details: POOH w/ 10 3/4in csg fish on spear until spear on surface" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 771m. The activity was categorized as 'plug abandon -- trip' and lasted for 0.2 hours. Operational details: Pulled spear assy and set casing fish in slips" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 771m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Released spear, inspected and R/B" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 771m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.8 hours. Operational details: R/U handling equipment for 10 3/4in casing" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 769m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Broke out 10 3/4in pup joint and L/D same" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 769m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Removed master bushing and installed FMS slips" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 769m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull 10 3/4in csg" "On 2016-08-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 410m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 3.0 hours. Operational details: POOH with 10 3/4in casing from 769m to 410 m. Average 10,7 joints/hr. Max 13 joints/hr Inspected perforated csg joint. Good flow area through perforation is observed" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 230m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.5 hours. Operational details: POOH with 10 3/4in casing from 410m to 230 m. Average pulling speed 12 joints/hr. Max 14 joints/hr. Totally 50x joints pulled" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 230m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Removed FMS slips, installed master bushing" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 2.2 hours. Operational details: POOH with 10 3/4in casing from 410m to surface. Used manual slips and dog collar. Average pulling speed 8 joints/hr. Totally 68x joints pulled" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to R/D csg handling equipment" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 1.0 hours. Operational details: R/D handling equipment for 10 3/4in csg" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- equipment recovery' and lasted for 0.5 hours. Operational details: Cleaned and cleared rig floor. TBT for BHA handling" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 1.0 hours. Operational details: M/U combined EZSV/cutting BHA (run#29)" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to change/adjust knives and use rig tongs" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Changed/adjust knives. Meanwhile cleared rig floor for csg equipment" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 2.0 hours. Operational details: Broke spear assembly. Attempted to make tongs to fit spear assembly" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Broke off taper mill, M/U Xover and EZSV running tool" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 57m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: M/U EZSV to running tool. RIH to 57m" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 57m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Installed PS21" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 902m. The activity was categorized as 'plug abandon -- other' and lasted for 3.5 hours. Operational details: RIH w/ EZSV-cutting BHA on 5,5in DP from 57m to 902m. Avg. tripping speed 240 m/hr" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 912m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Set EZSV at 912m w/ 36 turns to right. Took overpull in steps of 10t. Pulled free at 26t overpull. Set down 10t on EZSV. Pulled up 4m to extract setting tool" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 912m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Filled the string" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 912m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Filled the pipe more than expected. Checked surface equipment, pumps, lines, BOP and wellhead area. Observed level in the riser/BOP dropped around 20m. Lined up to trip tank and filled the well. Flow checked on trip tank. Attempted to fill string again. Total lost 11m3" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 912m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Recorded parameters for cutting: 600l/min - 74bar, 400l/min - 33,5bar, up/down weights 100t/94t" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 902m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.0 hours. Operational details: Cut 14in csg at 80rpm, 2-5kNm, 220l/min, 7 bar. Increased to 300l/min, 12bar, 2-10kNm, 80rpm, then 400l/min, 32bar Pressure slowly decreased to 11bar. Stopped pumping. Checked cut gap. Continued to cut to make sure csg is cut. Increased to 120rpm, 2-11kNm. Pressure dropped to 1bar. Casing cut @ 902m" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 902m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Circulated fluid in the well due to H2S readings in the return fluid on Baker sensor (7ppm)" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 902m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Flow checked well on trip tank. Well not static. Losses of 10,5m3/hour" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 902m. The activity was categorized as 'interruption -- repair' and lasted for 3.2 hours. Operational details: Evaluated situation. Meanwhile checked tension system on well head, Checked moon poll, well head, under cantilever for leals. No leaks observed. Stopped trip tank pump. Observed level in riser slowly dropping Meanwhile performed daily maintenance in red zone" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 902m. The activity was categorized as 'plug abandon -- cut' and lasted for 1.2 hours. Operational details: POOH w/ BHA (run#29) from 908m to 17m without filling the hole. Average pulling speed 712m/hour" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 17m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.5 hours. Operational details: Removed PS21 and installed master bushing, meanwhile performed TBT for BHA handling" "On 2016-08-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.8 hours. Operational details: L/D BHA (run#29)" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cut' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Changed BX inserts to 5in and prepared RTTS BHA components to P/U" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 74m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: M/U RTTS BHA and RIH with 2x stands of 8,25 DC to 74m" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: RIH w/ 2x stands of DP from 74m to 147m" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: M/U TDS and set RTTS packer at 147m" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Filled riser w/ 7.3m3. Observed level dropped in riser +/- 1 meter before stabilizing. Lined up TT pump and observed well - static" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed line test and closed BOP prior to pressure test above RTTS. Pressured up well to 6 bar and observe pressure bleeding off. Stop cement pump - pressure dropped to zero" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Opened BOP and monitored well on TT. TT level drop +/-1m3 over 20 min before stabilizing" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Attempted to pressure test again. Good low pressure test at 20bar/5min. Continued to pressured up to 25 bar and observed pressure bleeding off. Stopped cement pump and pressure dropped to zero" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 147m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Opened BOP and monitored well on TT. Observed loss rate 4.8m3/hr. Released RTTS packer, loss rate increased to 10.8m3/hr" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Picked up w/ RTTS packer to 142.5m (the depth above top shot of 10 3/4in csg perforation) Set RTTS at 142,5m. Well static. Pressure tested above RTTS to 20bar/5min and 50bar/5min. Good test. Released RTTS. Loss rate 10m3/hr" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: M/U new stand. RIH and RTTS packer at 155m. (the depth below bottom shot of 10 3/4in csg perforation) Loss rate 10m3/hr. Stopped TT pump and let level drop" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Filled pipe, performed line test. Attempted to pressure test below RTTS. No success. Pumped 1 m3, not able to achieve pressure build up" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 155m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Released RTTS" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 8m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: POOH on DP from 155m to 8m" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Changed inserts in elevator" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: L/D RTTS BHA" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared rig floor" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 3.2 hours. Operational details: Evaluated situation. Discussed situation w/ onshore organisation. Agreed way forward to attempt to cure losses w/ LCM pill Meanwhile serviced drilling equipment. Housekeeping. Adjusted link tilt, Performed maintenance on PS21, TDS, greased both PRSs." "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: Filled the well w/ sea water, observed returns at surface after 8,7 m3 pumped. Prepared and start mixing 400kg/m3 LCM pill in pump room" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.2 hours. Operational details: Continued mixing 400kg/m3 LCM pill in pump room. Hopper is packing off while mixing. Continued to mix manually. Worked good Flow checked on TT. Loss rate 10m3/hr" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.5 hours. Operational details: Continued mixing 400kg/m3 LCM pill in pump room Changed handling equipment and prepared to RIH w/ drill pipe" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 845m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: Continued mixing 400kg/m3 LCM pill in pump room RIH w/ 5,5in DP from surface to 845m" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 845m. The activity was categorized as 'interruption -- lost circulation' and lasted for 5.5 hours. Operational details: Continued mixing LCM pill while monitoring well. Loss rate 11m3/hrs. Meanwhile isolated and removed suction strainers in MP#2" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 900m. The activity was categorized as 'interruption -- lost circulation' and lasted for 2.0 hours. Operational details: Pumped 15m3 1.3sg 400kg/m3 LCM pill @ 550 LPM. When pill starts to exit string, decreased pump rate to 160l/min. Lined up TT and kept volume in TT static by adjusting pump rate between 160-200l/min to avoid LCM going up annulus and avoid SW from annulus dropping down and mix with LCM. Pumped and pulled to top of stand when +/- 2 m3 LCM left in the DP string. Stopped pumping after all LCM volume out of the DP string. Loss rate during pumping and displacing LCM pill +/- 11m3/hr" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 900m. The activity was categorized as 'interruption -- lost circulation' and lasted for 0.8 hours. Operational details: Stop pumping and monitor well on TT for 30 min. Loss rate +/- 10 m3/hr" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: POOH w/ 5,5in DP from 900m to surface. Average pulling speed 1200 m/hour" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Removed PS21, installed master bushing" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to RIH w/ RTTS" "On 2016-08-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 88m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: M/U RTTS BHA from surface to 88m" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 126m. The activity was categorized as 'interruption -- other' and lasted for 1.5 hours. Operational details: M/U RTTS BHA from 88 to 126m" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: RIH w/ RTTS slowly to 142m" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Set RTTS packer at 142m. Release setting tool from RTTS. 3x stands of 8 1/4in DC and 1x stand of 6 3/4in DC left hanging under RTTS (18ton)" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 142m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: Lined up and pressure tested RTTS packer from above 20bar/5min and 50bar/5min" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: POOH w/ 5,5in DP. L/D RTTS setting tool" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull diverter" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Prepared to N/D diverter. Removed BX-elevator, installed chains for pulling diverter. Bled off diverter system" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Removed MB and outer ring" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed lifting eyes to top of diverter. Loosened studs on bell nipple" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Attempted to pull diverter. No success. Pulled 10t overpull, diverter not moving. Troubleshoot same, removed eye bolts and cleaned, continued to attempt to pull diverter" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to pull diverter" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Attempted to pull diverter. Max 15t overpull. No success. Discussed plan forward" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.0 hours. Operational details: Disconnected NT2 connector and loosened slick joint. Loadshifted BOP from tensioning system to BOP carrier" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 1.5 hours. Operational details: Attempted to pull diverter w/ max 15t overpull. Lifted BOP and observed slick joint loosened in overshot. Cleaned around hold down dogs and observed one dog slightly engaged. Wedged in hold down dog and pulled diverter up passed dogs. Max overpull 12 Ton" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled diverter to rig floor. Installed master bushing and secured diverter on drill floor" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled slick joint. Prepared to disconnect tension system" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed tension cylinder and prepared to lift and skid BOP" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Lifted BOP and skidded to stump. Landed on stump" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed scaffolding in moon pool. Meanwhile M/U NT2 connector" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed master bushing and lowered down chain from TDS, made up to HPR. Meanwhile loosened connector on well head (HPR). Same time removed scaffolding under BOP stump" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled HPR to drillfloor and installed master bushing" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed Pre-job Meeting to L/D HPR using crane to tail out and back up tugger" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: LD HPR. Meanwhile strated to prepare to skid cantilever" "On 2016-08-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Installed cover on top deck in moon pool and lower deck. Meanwhile removed lifting equipment from TDS. CONTINUED REPORTING ON 15/9-F-12" "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Prepared for skidding. Removed hatched in moonpool. Meanwhile: Checked all skidding areas." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding operation." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Skidded rig from well F-5 to F-14." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.5 hours. Operational details: Installed cantilever access stairs. Performed post-skidding checks." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Removed hatch on F-5. Installed halfmoon hatch." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled master bushing and outer ring." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed HP riser. M/U connector between HP riser and WH. Detached HP riser lifting equipment and pulled same to drill floor." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed master bushing and outer ring. Meanwhile: Performed TBT with scaffolders" "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Built scaffolding around HP riser. Meanwhile: Prepared diverter and slipjoint." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued building scaffolding around riser. Meanwhile: Cleaned cement from inside of diverter" "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Moved BOP over well center" "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Checked cantilever alignment over well center. Skidded rig 4' aft to align HP riser and BOP." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Landed BOP on riser." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: M/U connector between BOP and HP riser. Meanwhile: Aligned tension cylinders with BOP." "On 2016-09-11, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed tension cylinders" "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Continued installing tension cylinders." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed master bushing. Installed slip joint" "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Installed master bushing. M/U nuts on slipjoint. Meanwhile: Prepared to install diverter." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed master bushing Installed diverter" "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D lifting equipment for diverter. Installed BX-4 elevator." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pressurized BOP control system." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Filled riser, BOP and diverter with clean SW from trip tank." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for connector test" "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Attempted to pressure test BOP connector to 20/90 bar for 5/10min. Leakage observed on DHSV control line port on WH. Closed needle valve on DHSV control line port and installed blind plug." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Performed BOP connector test to 20/90 bar for 5/10min." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: P/U RTTS RT. Inspected and serviced tool." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 134m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ RTTS RT on 5 1/2' DP from surface to 134,5 m." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 134m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Closed annular preventer. Attempted to take up/down weight, not enough weight of DP to strip through annular. Opened annular preventer." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 134m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Attempted to sting into RTTS while pumping 90 lpm. No pressure increase observed." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 134m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.2 hours. Operational details: Increased flow rate to 150 lpm. Stung into RTTS packer and M/U 20 turns / 2500 Nm. No pressure in string observed." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 246m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Closed annular preventer and lined up to monitor pressure. Released RTTS packer, 25 ton OP. No pressure observed below RTTS packer. Opened annular preventer. Losses 13 m3/hr static." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 111m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: POOH w/ RTTS packer on 5 1/2' DP from 134 m to 111m." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 111m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: M/U lift sub and L/D the RTTS packer and RT." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 111m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed handling equipment for handling 6 3/4' DC." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 83m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: L/O singles 6 3/4' DC while POOH from 111 m to 83 m." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 83m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Changed handling equipment for handling 8 1/2' DC." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: L/O singles 8 1/2' DC while POOH from 83 m to surface." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 6m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: P/U 14' EZSV plug and pup. M/U BHA." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 84m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ 14' EZSV plug on 5 1/2' DP from 6 m to 84 m. Restricted running speed 2 min/std." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 84m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed master bushing. Installed PS-21 slips." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 866m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Continued RIH w/ 14' EZSV plug on 5 1/2' DP from 84 m to 866 m. Restricted running speed 2 min/std." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 866m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled PS-21 slips. Installed master bushing." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 866m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pumping brine and cement." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 891m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: RIH w/ 14' EZSV plug on 5 1/2' DP from 866 m to 891 m. Restricted running speed 2 min/std" "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Took up/down weight 96/90 ton. Set 14' EZSV plug at 892 m. Tagged EZSV w/ 5 ton. Meanwhile: Lined up for pumping brine." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/D single 5 1/2' DP. P/U and M/U 1,5m pup joint and pump-in sub. M/U cement hose and lo-torque valve." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Leak tested from cement unit against lo-torque on pump-in sub to 100 bar." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: Closed UPR and staged up pumps. 200 lpm / 3 bar, 300 lpm / 7 bar, 500 lpm / 36 bar. At 750 lpm the SPP increased to 81 bar, then dropped to 41 bar. SPP slowly increased to 60 bar and remained stable between 58 bar and 60 bar." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pumped 15 m3 1,36sg CaCl2 brine at 750 lpm / 61 bar. SPP decreased gradually to 37 bar at the end." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Displaced brine by pumping 11,2 m3 of SW at 750 lpm / 37 bar. SPP increased gradually to 48 bar at the end. Stopped pumping" "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Monitored for pressure build up. SPP 4,6 bar after shutting down pumps. Bled off to trip tank. No increase in TT observed." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Evaluated pressure trends. Loss zone above 14' casing cut." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Performed TBT for cement job." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Prepared for cement job on drill floor and pump room." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Pumped 20 m3 wash pill at 750 lpm. SPP increased to 78 bar. Decreased flow rate to 660 lpm, pressure stabilized at 75 bar." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Stopped pumps and observed 17 bar back pressure. Evaluated situation. Back pressure indicated heavy fluid moving upwards in annulus." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Pumped SW down drillstring, taking returns through choke into pit. Pumped 11 m3 SW before observing returns. After returns, pumped with 600 lpm / 11,9 bar. 66% return." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Closed choke and IBOP. Applied 20 bar behind IBOP. Applied 20 bar from cement unit to lo-torque on pump-in sub. Opened lo-torque and confirmed line-up." "On 2016-09-12, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 0.8 hours. Operational details: Mixed and pumped 14m3 1,95sg cement slurry at 600 lpm. Added well life 10kg/m3. Displaced cement with 12,2 m3 SW at 750 lpm from cement unit." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 892m. The activity was categorized as 'plug abandon -- squeeze' and lasted for 0.2 hours. Operational details: Continued displacing cement w/ 12,2 m3 SW. Stopped pumping. Observed 14 bar back pressure in DP, no pressure on annulus." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Opened BOP and stung out of EZSV plug. B/O and L/D pump-in sub. Installed sponge ball and pumped 9,5 m3 SW at 1500 lpm / 7 bar." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 850m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: R/B 1 std. Dropped 3' drift." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Removed master bushing. Installed PS-21 slips. Turned off TT pump" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 850 m to surface. Average pulling speed 680 m/hr." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Removed drift. Installed master bushing" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: L/D EZSV RT. Found 1 bow on EZSV RT bow-centralizer missing." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.0 hours. Operational details: WOC Meanwhile: Serviced drilling equipment." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 3.5 hours. Operational details: WOC Meanwhile: - Serviced drilling equipment and prepared fishing tools - Removed masterbushing and inspected diverter and BOP for lost centralizer piece. No findings. - Performed periodic maintenace on drilling equipment" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Performed TBT for building magnet BHA and retrieving centralizer piece." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 7m. The activity was categorized as 'interruption -- wait' and lasted for 1.5 hours. Operational details: WOC Meanwhile: P/U casing hanger mill assy. B/O string magnet, L/D milling assy. Installed bitsub and flat bottom magnet in fox hole. M/U magnet BHA in rotary." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 7m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Removed master bushing. Installed PS-12 slips" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 879m. The activity was categorized as 'interruption -- wait' and lasted for 1.8 hours. Operational details: WOC Meanwhile: RIH w/ magnet BHA on 5 1/2' DP from 7 m to 879m. Restricted running speed 2 min/std." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 889m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Recorded up/down weight 95/89 ton. Continued RIH, took 12 ton weight 2,5 m shallower than EZSV plug at 889m Observed WOB decreased, possibly soft cement on top of EZSV plug." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 47m. The activity was categorized as 'interruption -- wait' and lasted for 1.2 hours. Operational details: WOC Meanwhile: POOH w/ magnet BHA on 5 1/2' DP from 889 m to 47 m. Restricted pulling speed 2 min/std." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 47m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Removed PS-21 slips. Installed master bushing." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 7m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: POOH w/ magnet BHA on 5 1/2' DP from 47 m to 7 m." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Insptected magnets, no centralizer piece found. Found cement residues on bottom magnet." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: B/O bitsub and flat bottom magnet. L/D BHA." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: WOC Meanwhile: R/U equipment for handling guns." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Performed TBT for handling explosives" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- wait' and lasted for 1.0 hours. Operational details: WOC Meanwhile: P/U and M/U 14' perforation guns." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 108m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: WOC Meanwhile: RIH w/ 14' guns on 5 1/2' DP to 108m" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 108m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Performed TBT with ongoing crew" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 148m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Continued RIH w/ 14' guns on 5 1/2' DP from 108 m to 147,5 m. Recorded up/down weight 71/67 ton. P/U XO and M/U TDS" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 148m. The activity was categorized as 'interruption -- wait' and lasted for 0.5 hours. Operational details: WOC Meanwhile: Filled well from trip tank. No losses observed. Closed UPR Confirmed line-up and filled pipe." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 148m. The activity was categorized as 'interruption -- wait' and lasted for 0.8 hours. Operational details: WOC Meanwhile: Opened UPR and B/O TDS. Dropped ball. M/U TDS and closed UPR. Pumped with 160 lpm. Guns fired at 132 bar SPP, perforation interval: 144,5m - 147,5m. Continued to circulate w/ 160 lpm / 3 bar. Increased flow rate in steps to 1000 lpm / 10 bar. Observed losses. Reduced rate to 750 lpm / 6 bar, loss rate 12 m3/hr. Max 0,65% gas during circulation in gas trap. Circulated 2,5 x B/U, until decreasing gas trend." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 148m. The activity was categorized as 'interruption -- wait' and lasted for 0.2 hours. Operational details: WOC Meanwhile: Opened UPR Flowchecked well for 10 min, static losses 12 m3/hr." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: POOH w/ 14' guns on 5 1/2' DP from 147,5 m to 28m." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 28m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Changed handling equipment to handle guns" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: L/D perforation guns and XO." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Cleaned and cleared drill floor Changed handling equipment." "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Performed TBT for cutting 14' casing" "On 2016-09-13, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: P/U 14' cutter BHA. Replaced 12 1/8' gauge stab with 12' string mill. Checked knifes and secured same." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Continued M/U 14' cutter BHA" "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Removed master bushing. Installed PS-21 slips." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 170m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: RIH w/ 14' cutter BHA on 5 1/2' DP from surface to 170m. RIH restricted until BHA below 14' subsea casing hanger." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'interruption -- repair' and lasted for 1.0 hours. Operational details: RIH w/ 14' cutter BHA on 5 1/2' DP from 170 m to 868 m. Avg running speed 840 m/hr." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'interruption -- repair' and lasted for 0.5 hours. Operational details: M/U TDS and filled pipe. Recorded up/down weight 96/92 ton. Recorded paramters." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 878m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Positioned cutter at 878m. Cut 14' casing at 878m, 450 lpm / 43 bar. Observed pressure drop in SPP, good indication of cut. Pulled up 1m with flow, observed pressure increased. RIH slowly and measured 10 cm window." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 878m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Filled well from trip tank Flowchecked well, 12m3/hr static losses." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 170m. The activity was categorized as 'interruption -- repair' and lasted for 0.8 hours. Operational details: POOH w/ 14' cutter BHA on 5 1/2' DP from 878 m to 170 m . Avg. pulling speed 700 m/hr." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Continued POOH restricted until BHA at surface." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: Removed PS-21 slips. Installed master bushing" "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- repair' and lasted for 0.2 hours. Operational details: L/D cutter BHA" "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 1.0 hours. Operational details: P/U and M/U 14' EZSV plug. Inspected packer element." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Installed PS-21 slips." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 666m. The activity was categorized as 'interruption -- other' and lasted for 1.2 hours. Operational details: RIH w/ 14' EZSV plug on 5 1/2' DP from surface to 666 m. Restricted running speed 2 min/std." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 827m. The activity was categorized as 'interruption -- other' and lasted for 0.2 hours. Operational details: Continued RIH w/ 14' EZSV plug on 5 1/2' DP from 666 m to 827 m. Restricted running speed 2 min/std." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'interruption -- other' and lasted for 0.5 hours. Operational details: Established circulation and washed the setting area, 800 lpm. Installed 14' EZSV plug at 868 m. Load tested the plug with 5 T down weight." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'interruption -- other' and lasted for 0.8 hours. Operational details: B/O and R/B 1 stand. P/U and M/U pump-in sub. Stung into EZSV plug. Meanwhile: Filled well with trip tank." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.5 hours. Operational details: Performed TBT for injection test and cement job Meanwhile: Leak tested cement hose to 100 bar." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'plug abandon -- mechanical plug' and lasted for 0.8 hours. Operational details: Lined up and attempted to perform injection test. SPP increased immediately to 20 bar, stopped pumps. Checked line-up. Lined up to cement hose, applied 20 bar and opened lo-torqe, no pressure drop observed. Correct line-up. Bled off pressure." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Performed 20 bar pressure test down DP/below EZSV plug from cement unit. Pressure leaked off slowly. Meanwhile: Filled hole (annulus) with trip tank pump, filled 10,61 m3. Montored well on TT, 11 m3/hr static losses. No change in pressure on cement unit." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 868m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: Applied 5 bar pressure down drill string/below EZSV from cement unit. Observed stable pressure (5 bar) for 10 min. Closed UPR and lined up to pump down kill line and monitor pressure on choke. Staged up pumps to 300 lpm / 7 bar. Increased flow to 500 lpm / 37,4 bar/10 min. Observed pressure below EZSV increased from 5 bar to 6 bar. Stopped pumping down kill line, observed pressure below EZSV dropped back to 5 bar and stable. Concluded with good leak test of cement in annulus to 31,4 bar." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 866m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Stung out of EZSV plug and P/U 2 m." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 866m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Lined up and pumped 10m3 wash pill, 900 lpm / 3,5 bar. Placed 100m balanced cement plug on top of EZSV: Mixed and pumped 8,2 m3 1,95sg cement slurry, 600 lpm. Displaced cement with 8,3 m3 drill water from cement unit 940 lpm / 10 bar." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 866m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: B/O and L/O pump-in sub." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 700m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.0 hours. Operational details: POOH to 700m. M/U pup joint with pre-loaded sponge ball. Circulated SW until clean returns (less than 30ppm oil in water concentration) at 3500 lpm / 31 bar while rotating 50 rpm / 1 - 4 kNm. Pumped totally 75 m3 of SW." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 626m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 700 m to 626 m." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 626m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed master bushing." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 626m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 1.2 hours. Operational details: Installed FOSV and BOP wash tool. Jetted BOP 3 x passes at 1600 lpm / 14 bar, 60 rpm / 1 - 4 kNm. Functioned BOP rams Jetted BOP additional 3 x passes 1600 lpm / 14 bar, 60 rpm / 1 - 4 kNm. L/O BOP wash tool and FOSV." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 626m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: Installed PS-21 slips" "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 22m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.5 hours. Operational details: POOH w/ EZSV RT on 5 1/2' DP from 626 m to 22 m. Avg. pulling speed 1200 m/hr." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 22m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.2 hours. Operational details: Installed master bushing" "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- cement plug' and lasted for 0.8 hours. Operational details: L/D EZSV RT." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D rotator and elevator. R/U diverter chains and bridle." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for N/D BOP" "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.8 hours. Operational details: Removed master bushing Installed lifting equipment on diverter. Released bolts on slipjoint. Depressurized diverter system. Lifted diverter and slipjoint to drill floor." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Removed tension cylinders and disconnected BOP connector." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lifted BOP with carrier and skidded over to test stump." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Connected lifting equipment to hi-pressure riser. Removed scaffolding in moonpool and disconnected hi-pressure riser from WH. Meanwhile: Performed pre-skidding checks prior to skidding cantilever." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Lifted HP riser to drill floor." "On 2016-09-14, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed hatches in moonpool on well F-14. Installed master bushing." "On 2016-09-15, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Continued installing hatch on well F-14. ******** END OF REPORT *******" "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 0.2 hours. Operational details: Performed TBT for skidding rig to well F-14" "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'moving -- skid' and lasted for 1.5 hours. Operational details: Skidded cantilever to well F-14 Removed hatch. Built scaffolding in moonpool Installed hole covers on well F-15. Meanwhile: R/U return hoses." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: Pulled master bushing and lowered NT2 connector down to Multibowl. Installed NT2 connector to Multibowl. Changed to BX-elevator." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: P/U cutter BHA. B/O and R/B handling pup and pup joint." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: P/U and M/U Multibowl RT. RIH and engaged RT to Multibowl. Confirmed by taking 20 ton overpull." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/D tension cylinders" "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 2.5 hours. Operational details: Load shifted weight to TDS. R/D tension cylinders." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for R/D boat collision stool" "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/D boat collision stool and centralizer" "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Increased flow rate in steps to 2300 lpm / 82 bar. Cut riser at 134,9m" "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.0 hours. Operational details: R/D hoses and valve outlets from Multibowl." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser and inner string to drill floor. Removed master bushing and installed C-plate." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: B/O Multibowl RT and parked same in AFT PRS. Rigged up false rotary." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled inner string. R/B cutter BHA." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: M/U Multibowl RT and removed C-plate." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled Multibowl and tensioner joint. Stopped every meter to clean off marine growth on centralizer deck. Installed master bushing and elevator. Landed off riser onto elevator." "On 2016-10-18, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: R/U cutting machine Started cutting tensioner joint." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.2 hours. Operational details: Cut tensioner joint. Significant wave height 1 m. R/D cutter" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O tensioner joint (Lift #1)" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/D Multibowl RT and NT2 connector" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Pulled riser (Lift #2). Cleaned off marine growth on centralizer deck. Installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 1m. R/D cutting machine." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O splash zone joint and upper pup." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Pulled riser (Lift #3). Cleaned off marine growth on centralizer deck. Installed master bushing and elevator. Landed riser onto elevator." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine Cut riser. Significant wave height 0,9m R/D cutting machine." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (Lift #3)" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Pulled riser (Lift #4). Cleaned off marine growth on centralizer deck. Installed master bushing and elevator. Landed riser onto elevator. Riser out of splash zone at 05:30" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 1.5 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: Performed TBT for pull, cut and L/O riser" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: L/O riser joint (Lift #4) Latched onto elevator (Lift #5) Pulled riser. Landed same onto elevator." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (Lift #5) Latch onto riser (Lift #6) and pulled riser. Landed off riser onto elevator." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: R/U cutting machine Cut riser R/D cutting machine" "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.2 hours. Operational details: L/O riser joint (Lift #6). Pulled riser (Lift #7)." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.5 hours. Operational details: Removed master bushing and POOH with riser (Lift #7). L/O riser joint." "On 2016-10-19, at Well NO 15/9-F-14, a drilling event occurred at a depth of 0m. The activity was categorized as 'plug abandon -- other' and lasted for 0.8 hours. Operational details: Installed hatches. Removed scaffolding. Meanwhile: Completed skidding checklists. **** END OF REPORT ****"